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| number = ML11178A068 | | number = ML11178A068 | ||
| issue date = 06/23/2011 | | issue date = 06/23/2011 | ||
| title = | | title = Meeting Slides, Turkey Point Nuclear Plant, Units 3 and 4, Extended Power Uprate (Epu), NRC and FPL Public Meeting | ||
| author name = | | author name = | ||
| author affiliation = Florida Power & Light Co | | author affiliation = Florida Power & Light Co | ||
| addressee name = Paige J | | addressee name = Paige J | ||
| addressee affiliation = NRC/NRR/DORL/LPLII-2 | | addressee affiliation = NRC/NRR/DORL/LPLII-2 | ||
| docket = 05000250, 05000251 | | docket = 05000250, 05000251 | ||
| Line 14: | Line 14: | ||
| document type = Meeting Briefing Package/Handouts, Slides and Viewgraphs, Meeting Agenda | | document type = Meeting Briefing Package/Handouts, Slides and Viewgraphs, Meeting Agenda | ||
| page count = 21 | | page count = 21 | ||
| project = TAC:ME4907, TAC:ME4908 | |||
| stage = Meeting | |||
}} | }} | ||
=Text= | |||
{{#Wiki_filter:Agenda | |||
* Opening | |||
* Purpose | |||
* EPU License Amendment Request (LAR) Review Summary | |||
* Proposed Technical Specification Changes | |||
* Mechanical and Civil Outstanding Questions | |||
* Nuclear Performance and Code Review | |||
- Boron Precipitation Analysis Discussion | |||
* Containment and Ventilation EPITOME Analysis | |||
* Reactor Systems Branch Questions | |||
* Questions | |||
* Closing I=PL. | |||
2 | |||
Turkey Point -- Opening | |||
* Appreciate the Staff's support and participation today | |||
* Significant progress made to date | |||
* FPL seeks clarification and understanding of remaining Staff questions | |||
* Encourage open and active dialogue to address open items from the Staff's review a=pL. | |||
3 | |||
Turkey Point -- Purpose | |||
* Review status of Requests for Additional Information (RAls) | |||
* Discuss remaining questions and/or open items | |||
* Discuss "to go" plan for final draft safety evaluation (SE) to Advisory Committee on Reactor Safeguards (ACRS) 8 I=PL. | |||
4 | |||
EPU LAR Review Summary | |||
* 6 draft SEs are complete for the 17 branches | |||
* 4 draft SEs are in branch concurrence | |||
* Draft Environmental Assessment scheduled for 7/15/1 | |||
* Focus today is to resolve any questions and/or open items remaining | |||
- Technical Specifications - Confirm no questions or comments on proposed Technical Specifications Mechanical and Civil Engineering - Follow-up questions | |||
- Nuclear Performance and Code - PHOENIX-P/ANC benchmarking and boron precipitation | |||
- Containment and Ventilation - EPITOME issue | |||
- Reactor Systems - outstanding RAls and RETRAN deck F=PL, 5 | |||
e: | |||
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c.cu eJ: | |||
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Mechanical and Civil Engineering | |||
* Received 6 follow-up RAls on 6/20/11 | |||
- Spent Fuel Pool Cooling and Component Cooling Water modification design information | |||
- Normal containment cooler modification design information | |||
- Containment penetration anchor margins | |||
- Use of actual material properties for reactor vessel supports | |||
- Allowable stresses for control rod drive mechanisms | |||
- Steam Generator fluid steam mixture velocity information | |||
* Clarification discussion today | |||
* Preparing responses with a target of mid July 2011 I=PL. | |||
7 | |||
Nuclear Performance and Code Review | |||
* Providing additional information regarding PHOENIX-PlANe benchmarking - Target early July | |||
* Boric Acid Precipitation | |||
- Status of NRC confirmatory analysis Discuss and reach agreement on anticipated FPL actions based on lessons learned from the Point Beach EPU | |||
-- Summarize conservatisms in the analysis | |||
-- Provide additional discussion on operational considerations for small break LOCAs | |||
-- Confirmation that charging pumps trip on safety injection | |||
-- Provide at least 1 hour of margin between lineup for hot leg injection and the onset of boron precipitation | |||
-- Other actions? | |||
FPL. | |||
8 | |||
Nuclear Performance and Code Review Boric Acid Precipitation Timeline | |||
:s:: | |||
a u.. | |||
Cf) | |||
Injection Mode 1 RHR Pump, 2 HHSI Pumps | |||
/ | |||
Injection Mode 2 HHSI Pumps | |||
.j 1 hour and 10 minutes 1 | |||
Hot Leg Recircu ation Mode 2 HHSI Pumps 2 HHSI P umps Cold Leg Red,,"',,'oO Mode I.. | |||
*1 Time After LOCA H DelaY1 LT - RWST Low Low Level z | |||
Tl - RWST Low Level To - Event Initiation Tl - 15 minutes T - 45 minutes z | |||
To-Event Initation T3 - 5 hours, 30 minutes T. - 6 hours, 40 minutes DelaYl - 2 minutes (EPU) | |||
Delay T. - Incipient Boric Acid z l Precipitation Without Hot Leg Recirculation T3 - HLSO Initiation Delay - 3 minutes (EPU) z I=PL. | |||
9 | |||
Containment and Ventilation - EPITOME Analysis | |||
* EPITOME code error involves LOCA mass and energy release calculation | |||
* Turkey Point containment analysis is impacted | |||
* Plant operability has been addressed | |||
* EPU LOCA and MSLB analyses performed EPITOME code error correction Range for containment free volume | |||
* Technical specification change proposed to lower limit on normal operating containment pressure from 3 psig to. | |||
1 psig Include ITS improvement for administrative control of instrument air bleed 10 I=PL. | |||
Containment and Ventilation - EPITOME Analysis | |||
* Other changes Modify the Emergency Containment Cooler (ECC) Start Logic to ensure 2 ECCs operate (new commitment) | |||
Reduce upper operating band on Tav9 from 3°F to 1.soF Other input changes | |||
* Draft Results 11 I=PL. | |||
Containment and Ventilation - EPITOME LOCA Draft Results | |||
--- Containment Pressure. OEPS MINSI | |||
----- Containment Pressure, OEPS MINSI Rev ised r--... | |||
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6 7 | |||
a 10 10 10 10 10 10 10 10 10 Time (s) | |||
FPL. | |||
Containment and Ventilation - EPITOME MSLB Draft Results Containment Pressure. 1*0 sq ft Split | |||
----. Co n tainment Pressure. 1.0 sq ft Split Revised 60-'-'--------------------, | |||
50 | |||
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o 200 400 600 800 1000 Transient Time (sec) | |||
Con tai nmen t Temperature. 30 % Power DER MSCV | |||
----. Containment Temperature. HZP DER MSCV Revised 3511 ~\\ | |||
300 | |||
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~ | |||
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0 200 400 600 BOD 1000 Transient Time (sec) 13 FPL. | |||
Containment and Ventilation - EPITOME | |||
* Areas requiring revised analysis (applicable LAR sections in parentheses) | |||
Component Cooling Water Systems (2.5.4.3) | |||
Primary Containment Functional Design (2.6.1) | |||
Mass and Energy Release (2.6.3) | |||
Containment Heat Removal (2.6.5) | |||
* Determined to be acceptable 14 FPL. | |||
Containment and Ventilation - EPITOME | |||
* Other areas reviewed and determined no impact (applicable LAR sections in parentheses) | |||
Protective Coating Systems (2.1.7) | |||
Balance of Plant Piping, Components and Supports (2.2.2.2) | |||
Safety-Related Valves and Pumps (2.2.4) | |||
Environmental Qualification of Electrical Equipment (2.3.1) | |||
Pressure Analysis for ECCS Performance Capability (2.6.6) | |||
Containment Ventilation System (2.7.7) | |||
ECCS and Loss-of-Coolant Accidents (2.8.5.6.3) | |||
Radiological Consequences Analyses Using AST (2.9.2) | |||
* No change to LAR section conclusions for impact of EPU 15 FPL. | |||
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Reactor Systems Branch Questions | |||
* Received 31 non-LOCA RAls on 6/10/11 Conducted clarification call on 6/20/11 Preparing responses with a target issue of mid-July 2011 | |||
* Further discussion on the following: | |||
NUREG 0800 requirement regarding credited reactor trips for loss of load analysis | |||
- Analysis of credible main steam line breaks | |||
- eves malfunction in Modes 3, 4, and 5 (j | |||
17 I=PL. | |||
Reactor Systems Branch Questions | |||
* Received additional RAls: | |||
10on6/14/11 | |||
- 7on6/17/11 | |||
- Anticipate remaining questions by 6/23/11 | |||
- Clarification discussion today Preparing responses with a target of mid July 2011 | |||
* Further discussion on the following: | |||
Inadvertent opening of a PORV | |||
- Additional information regarding LBLOCA nodalization 18 FPL.. | |||
Reactor Systems Branch Questions | |||
* RETRAN Deck Modified Turkey Point base deck to be compatible with RETRAN3D | |||
- Westinghouse transmitted to NRC on 6/21/11 Personnel available today to assist the Staff with running RETRAN with the modified base deck to ensure its compatibility with Staff software 19 F=PL. | |||
3: | |||
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Turkey Point - Closing | |||
* FPL respond to remaining RAls and clarification requests | |||
* Staff to complete remaining draft SE input | |||
* Draft SE to ACRS Subcommittee in August | |||
* Prepare for ACRS Subcommittee meeting in September and ACRS Full Committee meeting in October 21 I=PL.}} | |||
Latest revision as of 05:41, 13 January 2025
| ML11178A068 | |
| Person / Time | |
|---|---|
| Site: | Turkey Point |
| Issue date: | 06/23/2011 |
| From: | Florida Power & Light Co |
| To: | Jason Paige Plant Licensing Branch II |
| Shared Package | |
| ML11195A170 | List: |
| References | |
| TAC ME4907, TAC ME4908 | |
| Download: ML11178A068 (21) | |
Text
Agenda
- Opening
- Purpose
- Proposed Technical Specification Changes
- Mechanical and Civil Outstanding Questions
- Nuclear Performance and Code Review
- Boron Precipitation Analysis Discussion
- Containment and Ventilation EPITOME Analysis
- Reactor Systems Branch Questions
- Questions
- Closing I=PL.
2
Turkey Point -- Opening
- Appreciate the Staff's support and participation today
- Significant progress made to date
- FPL seeks clarification and understanding of remaining Staff questions
- Encourage open and active dialogue to address open items from the Staff's review a=pL.
3
Turkey Point -- Purpose
- Review status of Requests for Additional Information (RAls)
- Discuss remaining questions and/or open items
- Discuss "to go" plan for final draft safety evaluation (SE) to Advisory Committee on Reactor Safeguards (ACRS) 8 I=PL.
4
- 6 draft SEs are complete for the 17 branches
- 4 draft SEs are in branch concurrence
- Draft Environmental Assessment scheduled for 7/15/1
- Focus today is to resolve any questions and/or open items remaining
- Technical Specifications - Confirm no questions or comments on proposed Technical Specifications Mechanical and Civil Engineering - Follow-up questions
- Nuclear Performance and Code - PHOENIX-P/ANC benchmarking and boron precipitation
- Containment and Ventilation - EPITOME issue
- Reactor Systems - outstanding RAls and RETRAN deck F=PL, 5
e:
+' ° ca U
II U(1),...
c.:::::s UJO
_-C cue:
ucu
-c J:
.c:(1)
(.)(1)
(1)UJ
~I tn (l)Q) tnc) 0e:
c.cu eJ:
D..O
<0
-C
Mechanical and Civil Engineering
- Received 6 follow-up RAls on 6/20/11
- Spent Fuel Pool Cooling and Component Cooling Water modification design information
- Normal containment cooler modification design information
- Containment penetration anchor margins
- Use of actual material properties for reactor vessel supports
- Allowable stresses for control rod drive mechanisms
- Steam Generator fluid steam mixture velocity information
- Clarification discussion today
- Preparing responses with a target of mid July 2011 I=PL.
7
Nuclear Performance and Code Review
- Providing additional information regarding PHOENIX-PlANe benchmarking - Target early July
- Boric Acid Precipitation
- Status of NRC confirmatory analysis Discuss and reach agreement on anticipated FPL actions based on lessons learned from the Point Beach EPU
-- Summarize conservatisms in the analysis
-- Provide additional discussion on operational considerations for small break LOCAs
-- Confirmation that charging pumps trip on safety injection
-- Provide at least 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> of margin between lineup for hot leg injection and the onset of boron precipitation
-- Other actions?
FPL.
8
Nuclear Performance and Code Review Boric Acid Precipitation Timeline
- s::
a u..
Cf)
Injection Mode 1 RHR Pump, 2 HHSI Pumps
/
Injection Mode 2 HHSI Pumps
.j 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> and 10 minutes 1
Hot Leg Recircu ation Mode 2 HHSI Pumps 2 HHSI P umps Cold Leg Red,,"',,'oO Mode I..
Tl - RWST Low Level To - Event Initiation Tl - 15 minutes T - 45 minutes z
To-Event Initation T3 - 5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />, 30 minutes T. - 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />, 40 minutes DelaYl - 2 minutes (EPU)
Delay T. - Incipient Boric Acid z l Precipitation Without Hot Leg Recirculation T3 - HLSO Initiation Delay - 3 minutes (EPU) z I=PL.
9
Containment and Ventilation - EPITOME Analysis
- EPITOME code error involves LOCA mass and energy release calculation
- Turkey Point containment analysis is impacted
- Plant operability has been addressed
- EPU LOCA and MSLB analyses performed EPITOME code error correction Range for containment free volume
- Technical specification change proposed to lower limit on normal operating containment pressure from 3 psig to.
1 psig Include ITS improvement for administrative control of instrument air bleed 10 I=PL.
Containment and Ventilation - EPITOME Analysis
- Other changes Modify the Emergency Containment Cooler (ECC) Start Logic to ensure 2 ECCs operate (new commitment)
Reduce upper operating band on Tav9 from 3°F to 1.soF Other input changes
- Draft Results 11 I=PL.
Containment and Ventilation - EPITOME LOCA Draft Results
--- Containment Pressure. OEPS MINSI
Containment Pressure, OEPS MINSI Rev ised r--...
(f)
D..
"-/
- J D1 IJ)
OJ OO~I----------------------------------~
5{)
.Q' 40
~ YJ n=20
..... :....//.-:\\\\...... :........ :........:........ :........
- \\
- \\
.......*......... :........ :.l.\\... :........ :........ :........ :........
- \\
- \\
\\
.....*.. :........ :........ :.... '\\i ' ~:'.\\'... :........ :........ :........
..*................................ :.. \\, '.'\\:........ :........:........
\\....
. \\ X ***** ** *** *** ** **
- 1Q1'.......................................... :...,,, ~.
oI
- 1111111, 11 11 1",
I! II,
I I ""'I
'I ""',
! '"1111 f IIII!I, 111""1
~
1 2
J
~
5
~
7 8
10 10 10 10 10 10 10 10 10 Time (3) 12 Contoinment Temperature. OEPS MINSI
Containment Temperoture, OEPS MINSI Revised jOO~I------------------------------------~
~
2 1;/\\
-.IlJ
\\. -...;' "...*....***...*. *.*.... *.*.., ***
l.L d
~,
'f 40
~
~
..2
~ 200 1.....*...................................~~....... :.....,.. :.......*
~
E OJ f-150-.......................,............................ -..................
I 11111111 1111111 1111111 1111111 11111111 11111111 11111111 11111111 100 I
I I
I I
I I
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1 2
j 4
~
6 7
a 10 10 10 10 10 10 10 10 10 Time (s)
FPL.
Containment and Ventilation - EPITOME MSLB Draft Results Containment Pressure. 1*0 sq ft Split
. Co n tainment Pressure. 1.0 sq ft Split Revised 60-'-'--------------------,
50
~
.12' 40 (J)
Q
'---./
~ 30
- s (J)
(J)
Q) ct 20 10 O +I~~~~~~~~~~~-L~~~~_.~--L-~
o 200 400 600 800 1000 Transient Time (sec)
Con tai nmen t Temperature. 30 % Power DER MSCV
. Containment Temperature. HZP DER MSCV Revised 3511 ~\\
300
/"'. 250 LL
~
- J 200
+-'
0 L
~ 150 E
Q)
I 100 50 0
0 200 400 600 BOD 1000 Transient Time (sec) 13 FPL.
Containment and Ventilation - EPITOME
- Areas requiring revised analysis (applicable LAR sections in parentheses)
Component Cooling Water Systems (2.5.4.3)
Primary Containment Functional Design (2.6.1)
Mass and Energy Release (2.6.3)
Containment Heat Removal (2.6.5)
- Determined to be acceptable 14 FPL.
Containment and Ventilation - EPITOME
- Other areas reviewed and determined no impact (applicable LAR sections in parentheses)
Protective Coating Systems (2.1.7)
Balance of Plant Piping, Components and Supports (2.2.2.2)
Safety-Related Valves and Pumps (2.2.4)
Environmental Qualification of Electrical Equipment (2.3.1)
Pressure Analysis for ECCS Performance Capability (2.6.6)
Containment Ventilation System (2.7.7)
ECCS and Loss-of-Coolant Accidents (2.8.5.6.3)
Radiological Consequences Analyses Using AST (2.9.2)
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<D
Reactor Systems Branch Questions
- Received 31 non-LOCA RAls on 6/10/11 Conducted clarification call on 6/20/11 Preparing responses with a target issue of mid-July 2011
- Further discussion on the following:
NUREG 0800 requirement regarding credited reactor trips for loss of load analysis
- Analysis of credible main steam line breaks
- eves malfunction in Modes 3, 4, and 5 (j
17 I=PL.
Reactor Systems Branch Questions
- Received additional RAls:
10on6/14/11
- 7on6/17/11
- Anticipate remaining questions by 6/23/11
- Clarification discussion today Preparing responses with a target of mid July 2011
- Further discussion on the following:
Inadvertent opening of a PORV
- Additional information regarding LBLOCA nodalization 18 FPL..
Reactor Systems Branch Questions
- RETRAN Deck Modified Turkey Point base deck to be compatible with RETRAN3D
- Westinghouse transmitted to NRC on 6/21/11 Personnel available today to assist the Staff with running RETRAN with the modified base deck to ensure its compatibility with Staff software 19 F=PL.
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Turkey Point - Closing
- FPL respond to remaining RAls and clarification requests
- Staff to complete remaining draft SE input