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| number = ML113140169
| number = ML113140169
| issue date = 11/09/2011
| issue date = 11/09/2011
| title = IR 05000458-11-004; on 07/01/2011 09/30/2011; River Bend Station; Integrated Resident and Regional Report; Postmaintenance Testing
| title = IR 05000458-11-004; on 07/01/2011 09/30/2011; River Bend Station; Integrated Resident and Regional Report; Postmaintenance Testing
| author name = Gaddy V G
| author name = Gaddy V
| author affiliation = NRC/RGN-IV/DRP/RPB-C
| author affiliation = NRC/RGN-IV/DRP/RPB-C
| addressee name = Olson E W
| addressee name = Olson E
| addressee affiliation = Entergy Operations, Inc
| addressee affiliation = Entergy Operations, Inc
| docket = 05000458
| docket = 05000458
Line 18: Line 18:


=Text=
=Text=
{{#Wiki_filter:
{{#Wiki_filter:November 9, 2011  
[[Issue date::November 9, 2011]]


Eric Site Vice President Entergy Operations, Inc.
Eric Site Vice President Entergy Operations, Inc.


River Bend Station 5485 US Highway 61
River Bend Station 5485 US Highway 61 St. Francisville, LA 70775


St. Francisville, LA 70775 Subject: RIVER BEND STATION  
Subject: RIVER BEND STATION - NRC INTEGRATED INSPECTION REPORT NUMBER 05000458/2011004
- NRC INTEGRATED INSPECTION REPORT NUMBER 05000458/2011004


==Dear Mr. Olson:==
==Dear Mr. Olson:==
On September 30, 2011, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your River Bend Station. The enclosed integrated inspection report documents the inspection findings, which were discussed on October 12, 2011, with you and other members of your staff.
On September 30, 2011, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your River Bend Station. The enclosed integrated inspection report documents the inspection findings, which were discussed on October 12, 2011, with you and other members of your staff.


The inspections examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
The inspections examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.
 
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.


Based on the results of this inspection, the NRC has identified two issues that were evaluated under the risk significance determination process as having very low safety significance (Green). The NRC has determined that a violation was associated with one of these issues.
Based on the results of this inspection, the NRC has identified two issues that were evaluated under the risk significance determination process as having very low safety significance (Green). The NRC has determined that a violation was associated with one of these issues.


However, because of the very low safety significance and because it was entered into your corrective action program, the NRC is treating this finding as a noncited violation, consistent with Section 2.3.2 of the NRC Enforcement Policy.
However, because of the very low safety significance and because it was entered into your corrective action program, the NRC is treating this finding as a noncited violation, consistent with Section 2.3.2 of the NRC Enforcement Policy. Additionally, five licensee-identified violations, which were determined to be of very low safety significance, are listed in this report.


Additionally, five licensee-identified violations, which were determined to be of very low safety significance, are listed in this report
If you contest the violations or the significance of the noncited violation, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, D.C.
. If you contest the violations or the significance of the noncited violation, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, D.C.


20555-0001, with copies to the Regional Administrator, U.S.
20555-0001, with copies to the Regional Administrator, U.S. Nuclear Regulatory Commission, Region IV, 612 E. Lamar Blvd, Suite 400, Arlington, Texas, 76011-4125; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, D.C. 20555-0001; and the NRC Resident Inspector at the River Bend Station facility. In addition, if you disagree with the crosscutting aspect assigned to any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region IV, and the NRC Resident Inspector at River Bend Station.


Nuclear Regulatory Commission, Region IV, 612 E. Lamar Blvd, Suite 400, Arlington, Texas, 76011
UNITED STATES NUCLEAR REGULATORY COMMISSION
-4125; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, D.C. 20555
-0001; and the NRC Resident Inspector at the River Bend Station facility. In addition, if you disagree with the crosscutting aspect assigned to any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region IV, and the NRC Resident Inspector at River Bend Station
. U N I T E D S T A T E S N U C L E A R R E G U L A T O R Y C O M M I S S I O N R E G I O N I V 6 12 EAST LAMAR BLVD
, S U I T E 4 0 0 A R L I N G T O N , T E X A S 7 6 0 1 1-4125 Entergy Operations, Inc. In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response, if you choose to provide one for cases where a response is not required, will be made available electronically for public inspection in the NRC Public Document Room or from the NRC's document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading
-rm/adams.html. To the extent possible, your response should not include any personal privacy or proprietary information so that it can be made available to the public without redaction.


Sincerely,RC Hagar for V G addy Vincent G. Gaddy, Chief Project Branch C Division of Reactor Projects Docket:
==REGION IV==
50-458 License: NPF-47
612 EAST LAMAR BLVD, SUITE 400 ARLINGTON, TEXAS 76011-4125


===Enclosure:===
Entergy Operations, Inc.
NRC Inspection Report 05000 458/2011004
 
- 2 -


===w/Attachment:===
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response, if you choose to provide one for cases where a response is not required, will be made available electronically for public inspection in the NRC Public Document Room or from the NRC's document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html. To the extent possible, your response should not include any personal privacy or proprietary information so that it can be made available to the public without redaction.
Supplemental Information cc w/


===Enclosure:===
Sincerely, RC Hagar for V Gaddy Vincent G. Gaddy, Chief Project Branch C Division of Reactor Projects
Distribution via Listserv


Entergy Operations, Inc. Electronic distribution by RIV:
Docket: 50-458 License: NPF-47


Regional Administrator (Elmo.Collins@nrc.gov
===Enclosure:===
) Deputy Regional Administrator (Art.Howell@nrc.gov)
NRC Inspection Report 05000458/2011004 w/Attachment: Supplemental Information
DRP Director (Kriss.Kennedy@nrc.gov
) DRP Deputy Director (Troy.Pruett@nrc.gov)
DRS Director (Anton.Vegel@nrc.gov) DRS Deputy Director (Tom.Blount@nrc.gov)
Senior Resident Inspector (Grant.Larkin@nrc.gov
) Branch Chief, DRP/C (Vincent.Gaddy@nrc.gov
) Resident Inspector (Andy.Barrett@nrc.gov)
RBS Administrative Assistant (Lisa.Day@nrc.gov)
Senior Project Engineer, DRP/C (Bob.Hagar@nrc.gov) Project Engineer, DRP/C (Rayomand.Kumana@nrc.gov
) Project Engineer, DRP/C (Jonathan.Braisted@nrc.gov)
Public Affairs Officer (Victor.Dricks@nrc.gov
) Public Affairs Officer (Lara.Uselding@nrc.gov
) Project Manager (Alan.Wang@nrc.gov)
Acting Branch Chief, DRS/TSB (Dale.Powers@nrc.gov)
RITS Coordinator (Marisa.Herrera@nrc.gov
) Regional Counsel (Karla.Fuller@nrc.gov
) Congressional Affairs Officer (Jenny.Weil@nrc.gov)
OEMail Resource ROPreports RIV/ETA: OEDO (Mark.Franke@nrc.gov) DRS/TSB STA (Dale.Powers@nrc.gov
) R:\_REACTORS\RBS\2011RBS2011004
-RP-GFL.DOCX SUNSI Rev Compl.


Yes No ADAMS Yes No Reviewer Initials vgg Publicly Avail Yes No Sensitive Yes No Sens. Type Initials vgg SRI:DRP/C RI:DRP/C SPE:DRP/C C:DRS/EB1 C:DRS/EB2 GFLarkin AJBarrett RCHagar TRFarnholtz NFO'Keefe RCH for GFL RCH for AJB
REGION IV==
/RA/ GGeroge for
Docket:
/RA/ 11/9/11 11/7/11 11/7/11 11/4/11 11/8/11 C:DRS/OB C:DRS/PSB1 C:DRS/PSB2 AC:DRS/TSB C:DRP/C MCHaire MCHay GEWerner DAPowers VGGaddy /RA/ /Ra/ /RA/ /RA/ RCH for VGG 11/4/11 11/7/11 11/3/11 118/11 11/8/11  OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax Enclosure U.S. NUCLEAR REGULATORY COMMISSION REGION IV Docket: 05000 458 License: NPF-47 Report: 05000458/2011004 Licensee: Entergy Operations, Inc.
05000458 License:
NPF-47 Report:
05000458/2011004 Licensee:
Entergy Operations, Inc.


Facility: River Bend Station Location: 5485 U.S. Highway 61 St. Francisville, LA Dates: July 1 through September 30, 2011 Inspectors:
Facility:
River Bend Station Location:
5485 U.S. Highway 61 St. Francisville, LA Dates:
July 1 through September 30, 2011 Inspectors:
G. Larkin, Senior Resident Inspector, Project Branch C A. Barrett, Resident Inspector, Project Branch C R. Hagar, Senior Project Engineer, Project Branch C L. Ricketson, Senior Health Physicist, Plant Support Branch 2 B. Baca, Health Physicist, Technical Support Branch C. Alldredge, Health Physicist, Plant Support Branch 2 Approved By:
G. Larkin, Senior Resident Inspector, Project Branch C A. Barrett, Resident Inspector, Project Branch C R. Hagar, Senior Project Engineer, Project Branch C L. Ricketson, Senior Health Physicist, Plant Support Branch 2 B. Baca, Health Physicist, Technical Support Branch C. Alldredge, Health Physicist, Plant Support Branch 2 Approved By:
Vincent G. Gaddy, Chief, Project Branch C Division of Reactor Projects Enclosure  
Vincent G. Gaddy, Chief, Project Branch C Division of Reactor Projects  
 
- 2 -
Enclosure  


=SUMMARY OF FINDINGS=
=SUMMARY OF FINDINGS=
IR 05000458/2011004; 07/01/2011  
IR 05000458/2011004; 07/01/2011 - 09/30/2011; River Bend Station; Integrated Resident and


- 09/30/2011; River Bend Station; Integrated Resident and Regional Report; Postmaintenance Testing The report covered a 3
Regional Report; Postmaintenance Testing  
-month period of inspection by resident inspectors and an announced baseline inspection by region-based inspector s. One Green noncited violation s and one Green finding of significance were identified. The significance of most findings is indicated by their color (Green, White, Yellow, or Red) using Inspection Manual Chapter 0609, "Significance Determination Process."  The crosscutting aspect is determined using Inspection Manual Chapter 0310, "Components Within the Cross Cutting Areas."  Findings for which the significance determination process does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG
-1649, "Reactor Oversight Process," Revision 4, dated December 2006.


===A. NRC-Identified Findings and Self-Revealing Findings===
The report covered a 3-month period of inspection by resident inspectors and an announced baseline inspection by region-based inspectors. One Green noncited violations and one Green finding of significance were identified. The significance of most findings is indicated by their color (Green, White, Yellow, or Red) using Inspection Manual Chapter 0609, Significance Determination Process. The crosscutting aspect is determined using Inspection Manual Chapter 0310, Components Within the Cross Cutting Areas. Findings for which the significance determination process does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process,
Revision 4, dated December 2006.


===NRC-Identified Findings and Self-Revealing Findings===
===Cornerstone: Initiating Events===
===Cornerstone: Initiating Events===
*
: '''Green.'''
: '''Green.'''
The inspectors identified a self-revealing finding involving inadequate corrective actions in response to a failure in the main steam equalizing header drain bypass valve, resulting in a steam leak and an unplanned plant down power. Specifically, plant personnel failed to properly address the dual indication on the bypass valve and fluid flow through the valve caus ed water to flash to steam accelerating pipe wall erosion and piping failure
The inspectors identified a self-revealing finding involving inadequate corrective actions in response to a failure in the main steam equalizing header drain bypass valve, resulting in a steam leak and an unplanned plant down power. Specifically, plant personnel failed to properly address the dual indication on the bypass valve and fluid flow through the valve caused water to flash to steam accelerating pipe wall erosion and piping failure. The licensees immediate corrective actions were to identify, secure, and temporarily repair the steam leak. The licensee entered this issue into the licensees corrective action program as Condition Report CR-RBS-2011-04592.
. The licensee's immediate corrective actions were to identify, secure, and temporarily repair the steam leak.
 
The licensee entered this issue into the licensee's corrective action program as Condition Report CR
-RBS-2011-04592. The finding was more than minor because it was associated with the equipment performance attribute of the initiating events cornerstone and affected the cornerstone objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions during shutdown as well as power operations.


The inspectors reviewed the finding using Inspection Manual Chapter 0609, Appendix A, "Significance Determination of Reactor Inspection Findings for At-Power Situations."
The finding was more than minor because it was associated with the equipment performance attribute of the initiating events cornerstone and affected the cornerstone objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. The inspectors reviewed the finding using Inspection Manual Chapter 0609, Appendix A, Significance Determination of Reactor Inspection Findings for At-Power Situations. Based on the Phase 1 screening of the finding, the inspectors determined that the finding was of very low safety significance (Green) because it was not a loss of coolant accident initiator, did not contribute to both the likelihood of an initiating event and the likelihood that mitigating equipment or functions would not be available, nor increase the likelihood of an external event (seismic, flooding, or severe weather event). The apparent cause of the performance deficiency was that the control room and outage control center personnel presumed that the main control room dual indication for the valve was incorrect because previously valve operation successfully closed the valve. Consequently, this finding has a crosscutting aspect in the area of human performance associated with the decision-making component because station personnel did not use a systematic process to assess the condition of the bypass valve, and failed to verify the validity of the underlying assumptions that were used to justify operation with the valve having dual indications [H.1(a)](Section 4OA2).
 
Based on the Phase 1 screening of the finding, the inspectors determined that the finding was of very low safety significance (Green) because it was not a loss of coolant accident initiator, did not contribute to both the likelihood of an initiating event and the likelihood that mitigating equipment or functions would not be available, nor increase the likelihood of an external event (seismic, flooding
, or severe weather event)
. The apparent cause of the performance deficiency was that the control room and outage control center personnel presumed that the main control room dual indication for the valve was incorrect because previously valve operation successfully closed the valve
. Consequently, this finding has a crosscutting aspect in the area of human performance associated with the decision-making component because station personnel did not use a systematic process to assess the condition of the bypass valve, and failed to verify the validity of the underlying assumptions that were used to justify operation with the valve having dual indications
[H.1(a)](Section 4OA2).


===Cornerstone: Barrier Integrity===
===Cornerstone: Barrier Integrity===
*
: '''Green.'''
: '''Green.'''
The inspectors identified a noncited violation of 10 CFR Part 50, Appendix B, Criterion III "Design Control," for an inadequate calculation methodology used in determining standby gas treatment system operability.
The inspectors identified a noncited violation of 10 CFR Part 50,
 
Appendix B, Criterion III Design Control, for an inadequate calculation methodology used in determining standby gas treatment system operability. The inspectors found that the calculation neither considered instrument uncertainty nor applied a proper voltage drop from the breaker to the standby gas treatment system filter train heater. The licensee entered this issue into the licensees corrective action program as Condition Report CR-RBS-2011-07332.
The inspectors found that the calculation neither considered instrument uncertainty nor applied a proper voltage drop from the breaker to the standby gas treatment system filter train heater.


The licensee entered this issue into the licensee's corrective action program as Condition Report CR
The finding was more than minor because it was associated with the design control attribute of the Barrier Integrity Cornerstone to maintain radiological barrier functionality of standby gas treatment trains, and affected the cornerstone objective to provide reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents or events.
-RBS-2011-07332. The finding was more than minor because it was associated with the design control attribute of the Barrier Integrity Cornerstone to maintain radiological barrier functionality of standby gas treatment trains , and affected the cornerstone objective to provide reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents or events.


Specifically, operating the standby gas system filter train heaters without sufficient output power is detrimental to the charcoal filters ability to retain radioactive iodine. This could result in a greater amount of radiation release to the environment in the event of an accident
Specifically, operating the standby gas system filter train heaters without sufficient output power is detrimental to the charcoal filters ability to retain radioactive iodine. This could result in a greater amount of radiation release to the environment in the event of an accident. In accordance with Inspection manual Chapter 0609, Appendix A, Significance Determination of Reactor Inspection Findings for At-Power Situations, the Phase 1 significance determination process screening determined the finding to be only of very low safety significance (Green) because the finding only represented a degradation of the radiological barrier function provided for the standby gas treatment system.
. In accordance with Inspection manual Chapter 0609, Appendix A, "Significance Determination of Reactor Inspection Findings for At-Power Situations," the Phase 1 significance determination process screening determined the finding to be only of very low safety significance (Green) because the finding only represented a degradation of the radiological barrier function provided for the standby gas treatment system.


The apparent cause of this finding was the decision to develop an engineering evaluation that did not include instrument uncertainly and did not validate the correct voltage drop between the filter train heater feeder breaker and the heater elements. The finding has a crosscutting aspect in the area of human performance associated with the decision-making component because station personnel failed to use conservative assumptions when developing the modified output power methodology for operation of the standby gas treatment system filter heaters with only 8 of 9 heater elements installed [H.1(b)](1R19 b.2).
The apparent cause of this finding was the decision to develop an engineering evaluation that did not include instrument uncertainly and did not validate the correct voltage drop between the filter train heater feeder breaker and the heater elements. The finding has a crosscutting aspect in the area of human performance associated with the decision-making component because station personnel failed to use conservative assumptions when developing the modified output power methodology for operation of the standby gas treatment system filter heaters with only 8 of 9 heater elements installed [H.1(b)](1R19 b.2).


===B. Licensee-Identified Violations===
===Licensee-Identified Violations===
 
Five violations of very low safety significance, which were identified by the licensee, have been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensees corrective action program. These violations and corrective action tracking numbers are listed in Section 4OA7.
Five violations of very low safety significance, which were identified by the licensee, have been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensee's corrective action program. These violations and corrective action tracking numbers are listed in Section 4OA7.


=REPORT DETAILS=
=REPORT DETAILS=


===Summary of Plant Status===
===Summary of Plant Status===
River Bend Station began the inspection period at 100 percent rated thermal power. On July 8, 2011, the plant reduced reactor power to 66 percent to perform control rod insertion tests, perform turbine bypass valve testing, and complete a control rod sequence exchange.


River Bend Station began the inspection period at 100 percent rated thermal power.
The plant returned to full power on July 10, 2011. On September 23, 2011, the plant reduced reactor power to 61 percent to complete a control rod sequence exchange. The plant returned to full power on September 27, 2011, and remained at 100 percent reactor power for the remainder of the inspection period.
 
On July 8, 2011, the plant reduced reactor power to 66 percent to perform control rod insertion tests, perform turbine bypass valve testing, and complete a control rod sequence exchange.
 
The plant returned to full power on July 10, 2011. On September 23, 2011, the plant reduced reactor power to 61 percent to complete a control rod sequence exchange.
 
The plant returned to full power on September 27, 2011
, and remained at 100 percent reactor power for the remainder of the inspection period.


==REACTOR SAFETY==
==REACTOR SAFETY==
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and Emergency Preparedness
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and Emergency Preparedness
{{a|1R01}}
{{a|1R01}}
==1R01 Adverse Weather Protection==
==1R01 Adverse Weather Protection==
{{IP sample|IP=IP 71111.01}}
{{IP sample|IP=IP 71111.01}}
Summer Readiness for Offsite and Alternate
Summer Readiness for Offsite and Alternate-ac Power a.
-ac Power a. The inspectors performed a review of preparations for summer weather for selected systems, including conditions that could lead to loss
 
-of-offsite power and conditions that could result from high temperatures. The inspectors reviewed the procedures affecting these areas and the communications protocols between the transmission system operator and the plant to verify that the appropriate information was being exchanged when issues arose that could affect the offsite power system. Examples of aspects considered in the inspectors' review includ ed: Inspection Scope The coordination between the transmission system operator and the plant's operations personnel during off
The inspectors performed a review of preparations for summer weather for selected systems, including conditions that could lead to loss-of-offsite power and conditions that could result from high temperatures. The inspectors reviewed the procedures affecting these areas and the communications protocols between the transmission system operator and the plant to verify that the appropriate information was being exchanged when issues arose that could affect the offsite power system. Examples of aspects considered in the inspectors review included:
-normal or emergency events The explanations for the events The estimates of when the offsite power system would be returned to a normal state   The notifications from the transmission system operator to the plant when the offsite power system was returned to normal During the inspection, the inspectors focused on plant
Inspection Scope
-specific design features and the procedures used by plant personnel to mitigate or respond to adverse weather conditions. Additionally, the inspectors reviewed the Updated Safety Analysis Report and performance requirements for systems selected for inspection, and verified that operator actions were appropriate as specified by plan t-specific procedures. Specific documents reviewed during this inspection are listed in the attachment. The inspectors also reviewed corrective action program items to verify that the licensee was identifying adverse weather issues at an appropriate threshold and entering them into their corrective action program in accordance with station corrective action procedures. The inspectors' reviews focused specifically on the following plant systems:
* The coordination between the transmission system operator and the plants operations personnel during off-normal or emergency events
Emergency diesel generators Fancy Point switchyard These activities constitute completion of one readiness for summer weather effect on offsite and alternate
* The explanations for the events
-ac power sample as defined in Inspection Procedure
* The estimates of when the offsite power system would be returned to a normal state
* The notifications from the transmission system operator to the plant when the offsite power system was returned to normal  
 
During the inspection, the inspectors focused on plant-specific design features and the procedures used by plant personnel to mitigate or respond to adverse weather conditions. Additionally, the inspectors reviewed the Updated Safety Analysis Report and performance requirements for systems selected for inspection, and verified that operator actions were appropriate as specified by plant-specific procedures. Specific  
 
documents reviewed during this inspection are listed in the attachment. The inspectors also reviewed corrective action program items to verify that the licensee was identifying adverse weather issues at an appropriate threshold and entering them into their corrective action program in accordance with station corrective action procedures. The inspectors reviews focused specifically on the following plant systems:
* Emergency diesel generators
* Fancy Point switchyard  
 
These activities constitute completion of one readiness for summer weather effect on offsite and alternate-ac power sample as defined in Inspection Procedure 71111.01-05.
 
b.


==71111.01 - 05.==
No findings were identified.
b. No findings were identified.


Findings
Findings
{{a|1R04}}
{{a|1R04}}
==1R04 Equipment Alignments==
==1R04 Equipment Alignments==
{{IP sample|IP=IP 71111.04}}
{{IP sample|IP=IP 71111.04}}
Partial Walkdown a. The inspectors performed partial system walkdowns of the following risk
Partial Walkdown a.
-significant systems: Inspection Scope Reactor core isolation cooling system following system maintenance
 
The inspectors performed partial system walkdowns of the following risk-significant systems:
Inspection Scope
* Reactor core isolation cooling system following system maintenance
* Division 2 standby service water during Division 3 emergency core cooling system testing
* Standby gas treatment B during Division 1 surveillance
* Division 1 main steam positive leakage control system while Division 2 was out of service for unplanned maintenance and troubleshooting


Division 2 standby service water during Division 3 emergency core cooling system testing Standby gas treatment B during Division 1 surveillance
The inspectors selected these systems based on their risk significance relative to the reactor safety cornerstones at the time they were inspected. The inspectors attempted to identify any discrepancies that could affect the function of the system, and, therefore, potentially increase risk. The inspectors reviewed applicable operating procedures, system diagrams, Updated Safety Analysis Report, technical specification requirements, administrative technical specifications, outstanding work orders, condition reports, and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have rendered the systems incapable of performing their intended functions. The inspectors also inspected accessible portions of the systems to verify system components and support equipment were aligned correctly and operable. The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no obvious deficiencies. The


Division 1 main steam positive leakage control system while Division 2 was out of service for unplanned maintenance and troubleshooting The inspectors selected these systems based on their risk significance relative to the reactor safety cornerstones at the time they were inspected. The inspectors attempted to identify any discrepancies that could affect the function of the system, and, therefore, potentially increase risk. The inspectors reviewed applicable operating procedures, system diagrams, Updated Safety Analysis Report, technical specification requirements, administrative technical specifications, outstanding work orders, condition reports, and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have rendered the systems incapable of performing their intended functions. The inspectors also inspected accessible portions of the systems to verify system components and support equipment were aligned correctly and operable. The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no obvious deficiencies. The inspectors also verified that the licensee had properly identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the corrective action program with the appropriate significance characterization. Specific documents reviewed during this inspection are listed in the attachment.
inspectors also verified that the licensee had properly identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the corrective action program with the appropriate significance characterization. Specific documents reviewed during this inspection are listed in the attachment.


These activities constitute completion of four partial system walkdown sample s as defined in Inspection Procedure
These activities constitute completion of four partial system walkdown samples as defined in Inspection Procedure 71111.04-05.
 
b.


==71111.04 - 05.==
No findings were identified.
b. No findings were identified.


Findings
Findings
{{a|1R05}}
{{a|1R05}}
==1R05 Fire Protection==
==1R05 Fire Protection==
{{IP sample|IP=IP 71111.05}}
{{IP sample|IP=IP 71111.05}}
===.1 Quarterly Fire Inspection Tours===
===.1 Quarterly Fire Inspection Tours===
a.
The inspectors conducted fire protection walkdowns that were focused on availability, accessibility, and the condition of firefighting equipment in the following risk-significant plant areas:
Inspection Scope
* July 19, 2011, reactor core isolation cooling pump room, fire area AB-4/Z-1 and Z-2
* July 19, 2011, D-Tunnel, fire area AB-7
* July 29, 2011, radwaste building, 106-foot elevation, fire area RW-106
* August 14, 2011, auxiliary building, 141-foot elevation and 98-foot elevation
* August 16, 2011, normal switchgear building, 98-foot elevation and 123-foot elevation
The inspectors reviewed areas to assess if licensee personnel had implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant; effectively maintained fire detection and suppression capability; maintained passive fire protection features in good material condition; and had implemented adequate compensatory measures for out of service, degraded or inoperable fire protection equipment, systems, or features, in accordance with the licensees fire plan.
The inspectors selected fire areas based on their overall contribution to internal fire risk as documented in the plants Individual Plant Examination of External Events with later additional insights, their potential to affect equipment that could initiate or mitigate a plant transient, or their impact on the plants ability to respond to a security event. Using the documents listed in the attachment, the inspectors verified that fire hoses and extinguishers were in their designated locations and available for immediate use; that fire detectors and sprinklers were unobstructed; that transient material loading was


a. The inspectors conducted fire protection walkdowns that were focused on availability, accessibility, and the condition of firefighting equipment in the following risk
within the analyzed limits; and fire doors, dampers, and penetration seals appeared to be in satisfactory condition. The inspectors also verified that minor issues identified during the inspection were entered into the licensees corrective action program.
-significant plant areas:
 
Inspection Scope July 19, 2011, reactor core isolation cooling pump room, fire area AB-4/Z-1 and Z-2  July 19, 2011, D-Tunnel , fire area AB-7  July 29, 2011, radwaste building , 106-foot elevation, fire area RW-106  August 14, 2011, auxiliary building , 141-foot elevation and 98-foot elevation August 16, 2011, normal switchgear building , 98-foot elevation and 123-foot elevation  The inspectors reviewed areas to assess if licensee personnel had implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant; effectively maintained fire detection and suppression capability; maintained passive fire protection features in good material condition; and had implemented adequate compensatory measures for out of service, degraded or inoperable fire protection equipment, systems, or features, in accordance with the licensee's fire plan.
Specific documents reviewed during this inspection are listed in the attachment.


The inspectors selected fire areas based on their overall contribution to internal fire risk as documented in the plant's Individual Plant Examination of External Events with later additional insights, their potential to affect equipment that could initiate or mitigate a plant transient, or their impact on the plant's ability to respond to a security event. Using the documents listed in the attachment, the inspectors verified that fire hoses and extinguishers were in their designated locations and available for immediate use; that fire detectors and sprinklers were unobstructed; that transient material loading was within the analyzed limits; and fire doors, dampers, and penetration seals appeared to be in satisfactory condition. The inspectors also verified that minor issues identified during the inspection were entered into the licensee's corrective action program. Specific documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of five quarterly fire-protection inspection samples as defined in Inspection Procedure 71111.05-05.


These activities constitute completion of five quarterly fire
b.
-protection inspection sample s as defined in Inspection Procedure


==71111.05 - 05.==
No findings were identified.
b. No findings were identified.


Findings
Findings
{{a|1R07}}
{{a|1R07}}
==1R07 Heat Sink Performance==
==1R07 Heat Sink Performance==
{{IP sample|IP=IP 71111.07}}
{{IP sample|IP=IP 71111.07}}
a. The inspectors reviewed licensee programs, verified performance against industry standards, and reviewed critical operating parameters and maintenance records for the containment and auxiliary building unit coolers (both divisions)
a.
. The inspectors verified that performance tests were satisfactorily conducted for heat exchangers/heat sinks and reviewed for problems or errors; the licensee utilized the periodic maintenance method outlined in EPRI Report NP 7552, "Heat Exchanger Performance Monitoring Guidelines"; the licensee properly utilized biofouling controls; the licensee's heat exchanger inspections adequately assessed the state of cleanliness of their tubes; and the heat exchanger was correctly categorized under 10 CFR 50.65, "Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants.Specific documents reviewed during this inspection are listed in the attachment.
 
The inspectors reviewed licensee programs, verified performance against industry standards, and reviewed critical operating parameters and maintenance records for the containment and auxiliary building unit coolers (both divisions). The inspectors verified that performance tests were satisfactorily conducted for heat exchangers/heat sinks and reviewed for problems or errors; the licensee utilized the periodic maintenance method outlined in EPRI Report NP 7552, Heat Exchanger Performance Monitoring Guidelines; the licensee properly utilized biofouling controls; the licensees heat exchanger inspections adequately assessed the state of cleanliness of their tubes; and the heat exchanger was correctly categorized under 10 CFR 50.65, Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants. Specific documents reviewed during this inspection are listed in the attachment.


Inspection Scope These activities constitute completion of one heat sink inspection sample as defined in Inspection Procedure
Inspection Scope  


==71111.07 - 05.==
These activities constitute completion of one heat sink inspection sample as defined in Inspection Procedure 71111.07-05.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R11}}
{{a|1R11}}
 
==1R11 Licensed Operator==
==1R11 Licensed Operator Requalification Program==
{{IP sample|IP=IP 71111.11}}
a.


Requalification Program (71111.11)a. On August 31, 2011 , the inspectors observed a crew of licensed operators in the plant's simulator to verify that operator performance was adequate, evaluators were identifying and documenting crew performance problems, and training was being conducted in accordance with licensee procedures. The inspectors evaluated the following areas:
On August 31, 2011, the inspectors observed a crew of licensed operators in the plants simulator to verify that operator performance was adequate, evaluators were identifying and documenting crew performance problems, and training was being conducted in accordance with licensee procedures. The inspectors evaluated the following areas:
Inspection Scope Licensed operator performance Crew's clarity and formality of communications Crew's ability to take timely actions in the conservative direction Crew's prioritization, interpretation, and verification of annunciator alarms Crew's correct use and implementation of abnormal and emergency procedures
Inspection Scope
* Licensed operator performance
* Crews clarity and formality of communications
* Crews ability to take timely actions in the conservative direction
* Crews prioritization, interpretation, and verification of annunciator alarms
* Crews correct use and implementation of abnormal and emergency procedures
* Control board manipulations
* Oversight and direction from supervisors
* Crews ability to identify and implement appropriate technical specification actions and emergency plan actions and notifications


Control board manipulations Oversight and direction from supervisors Crew's ability to identify and implement appropriate technical specification actions and emergency plan actions and notifications The inspectors compared the crew's performance in these areas to pre
The inspectors compared the crews performance in these areas to pre-established operator action expectations and successful critical task completion requirements.
-established operator action expectations and successful critical task completion requirements.


Specific documents reviewed during this inspection are listed in the attachment.
Specific documents reviewed during this inspection are listed in the attachment.


These activities constitute completion of one quarterly licensed
These activities constitute completion of one quarterly licensed-operator requalification program sample as defined in Inspection Procedure 71111.11.
-operator requalification program sample as defined in Inspection Procedure 71111.11. b. No findings were identified.
 
b.
 
No findings were identified.


Findings
Findings
{{a|1R12}}
{{a|1R12}}
==1R12 Maintenance Effectiveness==
==1R12 Maintenance Effectiveness==
{{IP sample|IP=IP 71111.12}}
{{IP sample|IP=IP 71111.12}}
a. The inspectors evaluated degraded performance issues involving the following risk significant systems:
a.
Inspection Scope Safety-related structures and the structural monitoring program Low pressure core spray system In addition, the inspectors reviewed the biennial Maintenance Rule (a)(3) report per the inspection guidance document.


The inspectors reviewed events such as where ineffective equipment maintenance has resulted in valid or invalid automatic actuations of engineered safeguards systems and independently verified the licensee's actions to address system performance or condition problems in terms of the following:
The inspectors evaluated degraded performance issues involving the following risk significant systems:
Implementing appropriate work practices Identifying and addressing common cause failures Scoping of systems in accordance with 10 CFR 50.65(b)
Inspection Scope
Characterizing system reliability issues for performance
* Safety-related structures and the structural monitoring program
* Low pressure core spray system  


Charging unavailability for performance
In addition, the inspectors reviewed the biennial Maintenance Rule (a)(3) report per the inspection guidance document.


Trending key parameters for condition monitoring
The inspectors reviewed events such as where ineffective equipment maintenance has resulted in valid or invalid automatic actuations of engineered safeguards systems and independently verified the licensee's actions to address system performance or condition problems in terms of the following:
* Implementing appropriate work practices
* Identifying and addressing common cause failures
* Scoping of systems in accordance with 10 CFR 50.65(b)
* Characterizing system reliability issues for performance
* Charging unavailability for performance
* Trending key parameters for condition monitoring
* Ensuring proper classification in accordance with 10 CFR 50.65(a)(1) or -(a)(2)
* Verifying appropriate performance criteria for structures, systems, and components classified as having an adequate demonstration of performance through preventive maintenance, as described in 10 CFR 50.65(a)(2), or as requiring the establishment of appropriate and adequate goals and corrective actions for systems classified as not having adequate performance, as described in 10 CFR 50.65(a)(1)


Ensuring proper classification in accordance with 10 CFR 50.65(a)(1) or
-(a)(2)
Verifying appropriate performance criteria for structures, systems, and components classified as having an adequate demonstration of performance through preventive maintenance, as described in 10 CFR 50.65(a)(2), or as requiring the establishment of appropriate and adequate goals and corrective actions for systems classified as not having adequate performance, as described in 10 CFR 50.65(a)(1)
The inspectors assessed performance issues with respect to the reliability, availability, and condition monitoring of the system. In addition, the inspectors verified maintenance effectiveness issues were entered into the corrective action program with the appropriate significance characterization. Specific documents reviewed during this inspection are listed in the attachment.
The inspectors assessed performance issues with respect to the reliability, availability, and condition monitoring of the system. In addition, the inspectors verified maintenance effectiveness issues were entered into the corrective action program with the appropriate significance characterization. Specific documents reviewed during this inspection are listed in the attachment.


These activities constitute completion of three quarterly maintenance effectiveness sample s as defined in Inspection Procedure
These activities constitute completion of three quarterly maintenance effectiveness samples as defined in Inspection Procedure 71111.12-05.
 
b.


==71111.12 - 05.==
No findings were identified.
b. No findings were identified.


Findings
Findings
{{a|1R13}}
{{a|1R13}}
==1R13 Maintenance Risk Assessments and Emergent Work Control==
==1R13 Maintenance Risk Assessments and Emergent Work Control==
{{IP sample|IP=IP 71111.13}}
{{IP sample|IP=IP 71111.13}}
a. The inspectors reviewed licensee personnel's evaluation and management of plant risk for the maintenance and emergent work activities affecting risk
a.
-significant and safety
 
-related equipment listed below to verify that the appropriate risk assessments were performed prior to removing equipment for work:
The inspectors reviewed licensee personnel's evaluation and management of plant risk for the maintenance and emergent work activities affecting risk-significant and safety-related equipment listed below to verify that the appropriate risk assessments were performed prior to removing equipment for work:
Inspection Scope Control rod drive pump failed postmaintenance testing, July 1, 2011   Emergent work in Fancy Point switchyard, August 8, 2011 Planned maintenance on the control room fresh air system, August 29, 2011
Inspection Scope
* Control rod drive pump failed postmaintenance testing, July 1, 2011
* Emergent work in Fancy Point switchyard, August 8, 2011
* Planned maintenance on the control room fresh air system, August 29, 2011
* Planned maintenance on a service water cooling fan and heat exchanger, September 12, 2011
* Elevated risk during RHR maintenance and switchyard work, September 13, 2011
 
The inspectors selected these activities based on potential risk significance relative to the reactor safety cornerstones. As applicable for each activity, the inspectors verified that licensee personnel performed risk assessments as required by 10 CFR 50.65(a)(4)and that the assessments were accurate and complete. When licensee personnel performed emergent work, the inspectors verified that the licensee personnel promptly assessed and managed plant risk. The inspectors reviewed the scope of maintenance work, discussed the results of the assessment with the licensee's probabilistic risk analyst or shift technical advisor, and verified plant conditions were consistent with the risk assessment. The inspectors also reviewed the technical specification requirements and inspected portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met. Specific documents reviewed during this inspection are listed in the attachment.


Planned maintenance on a service water cooling fan and heat exchanger , September 12, 2011 Elevated risk during RHR maintenance and switchyard work, September 13, 2011  The inspectors selected these activities based on potential risk significance relative to the reactor safety cornerstones. As applicable for each activity, the inspectors verified that licensee personnel performed risk assessments as required by 10 CFR 50.65(a)(4) and that the assessments were accurate and complete. When licensee personnel performed emergent work, the inspectors verified that the licensee personnel promptly assessed and managed plant risk. The inspectors reviewed the scope of maintenance work, discussed the results of the assessment with the licensee's probabilistic risk analyst or shift technical advisor, and verified plant conditions were consistent with the risk assessment. The inspectors also reviewed the technical specification requirements and inspected portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met. Specific documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of five maintenance risk assessments and emergent work control inspection samples as defined in Inspection Procedure 71111.13-05.


These activities constitute completion of five maintenance risk assessments and emergent work control inspection sample s as defined in Inspection Procedure
b.


==71111.13 - 05.==
No findings were identified.
b. No findings were identified.


Findings
Findings
{{a|1R15}}
{{a|1R15}}
==1R15 Operability Evaluations==
==1R15 Operability Evaluations==
{{IP sample|IP=IP 71111.15}}
{{IP sample|IP=IP 71111.15}}
a. The inspectors reviewed the following issues:
a.
Inspection Scope CR-RBS-2011-04859, reactor core isolation cooling suction pressure high following high pressure core spray runs, reviewed on July 18, 2011 CR-RBS-2011-05439, reactor core isolation cooling turbine speed error during surveillance testing, reviewed on July 21, 2011 CR-RBS-2011-05597, diesel generator thermostatic valve problem not identified promptly, reviewed on July 21, 2011 CR-RBS-2011-06063, E12
 
-F048B flexible electrical conduit jacket degraded, reviewed on August 22, 2011 CR-RBS-2011-06387, main steam positive leakage compressor failures, reviewed on August 29, 2011 CR-RBS-2011-05395, inadequate design of auxiliary building penetration , reviewed on August 30, 2011 The inspectors selected these potential operability issues based on the risk significance of the associated components and systems. The inspectors evaluated the technical adequacy of the evaluations to ensure that technical specification operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the technical specifications and Updated Safety Analysis Report to the licensee personnel's evaluations to determine whether the components or systems were operable. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. The inspectors determined, where appropriate, compliance with bounding limitations associated with the evaluations.
The inspectors reviewed the following issues:
Inspection Scope
* CR-RBS-2011-04859, reactor core isolation cooling suction pressure high following high pressure core spray runs, reviewed on July 18, 2011
* CR-RBS-2011-05439, reactor core isolation cooling turbine speed error during surveillance testing, reviewed on July 21, 2011
* CR-RBS-2011-05597, diesel generator thermostatic valve problem not identified promptly, reviewed on July 21, 2011
* CR-RBS-2011-06063, E12-F048B flexible electrical conduit jacket degraded, reviewed on August 22, 2011
* CR-RBS-2011-06387, main steam positive leakage compressor failures, reviewed on August 29, 2011
* CR-RBS-2011-05395, inadequate design of auxiliary building penetration, reviewed on August 30, 2011  
 
The inspectors selected these potential operability issues based on the risk significance of the associated components and systems. The inspectors evaluated the technical adequacy of the evaluations to ensure that technical specification operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the technical specifications and Updated Safety Analysis Report to the licensee personnels evaluations to determine whether the components or systems were operable. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. The inspectors determined, where appropriate, compliance with bounding limitations associated with the evaluations.


Additionally, the inspectors also reviewed a sampling of corrective action documents to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations. Specific documents reviewed during this inspection are listed in the attachment.
Additionally, the inspectors also reviewed a sampling of corrective action documents to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations. Specific documents reviewed during this inspection are listed in the attachment.


These activities constitute completion of six operability evaluation inspection sample s as defined in Inspection Procedure
These activities constitute completion of six operability evaluation inspection samples as defined in Inspection Procedure 71111.15-04
 
b.


==71111.15 - 04==
No findings were identified.
b. No findings were identified.


Findings
Findings
{{a|1R18}}
{{a|1R18}}
==1R18 Plant Modifications==
==1R18 Plant Modifications==
{{IP sample|IP=IP 71111.18}}
{{IP sample|IP=IP 71111.18}}
a. Temporary Modifications To verify that the safety functions of important safety systems were not degraded, the inspectors reviewed the following temporary modifications:
a.
Inspection Scope Engineering Change EC
 
-31398, "LSV
Temporary Modifications To verify that the safety functions of important safety systems were not degraded, the inspectors reviewed the following temporary modifications:
-AOV44B Outlet Restricting Orifice," Revision 0; Engineering Change EC
Inspection Scope
-31483, "Remove Level Control Function for SWP-SOV220B," Revision 0; and Engineering Change EC
* Engineering Change EC-31398, LSV-AOV44B Outlet Restricting Orifice, Revision 0; Engineering Change EC-31483, Remove Level Control Function for SWP-SOV220B, Revision 0; and Engineering Change EC-31488, Revise References to LSV Separator Tank Levels in TMOD EC-31483, Revision 0
-31488, "Revise References to LSV Separator Tank Levels in TMOD EC
* Engineering Change EC-30850, GTS-FLT1B Operation with One Heater Element Out of Service, Revision 0  
-31483," Revision 0 Engineering Change EC
-30850, "GTS
-FLT1B Operation with One Heater Element Out of Service," Revision 0 The inspectors reviewed the temporary modification s and the associated safety
-evaluation screening against the system design bases documentation, including the Updated Safety Analysis Report and the technical specifications, and verified that the modification did not adversely affect the system operability/availability. The inspectors also verified that the installation and restoration were consistent with the modification documents and that configuration control was adequate. Additionally, the inspectors verified that the temporary modification was identified on control room drawings, appropriate tags were placed on the affected equipment, and licensee personnel evaluated the combined effects on mitigating systems and the integrity of radiological barriers. These activities constitute completion of two sample s for temporary plant modifications as defined in Inspection Procedure


==71111.18 - 05.==
The inspectors reviewed the temporary modifications and the associated safety-evaluation screening against the system design bases documentation, including the Updated Safety Analysis Report and the technical specifications, and verified that the modification did not adversely affect the system operability/availability. The inspectors also verified that the installation and restoration were consistent with the modification documents and that configuration control was adequate. Additionally, the inspectors verified that the temporary modification was identified on control room drawings, appropriate tags were placed on the affected equipment, and licensee personnel
b. No findings were identified.
 
evaluated the combined effects on mitigating systems and the integrity of radiological barriers.
 
These activities constitute completion of two samples for temporary plant modifications as defined in Inspection Procedure 71111.18-05.
 
b.
 
No findings were identified.


Findings
Findings
{{a|1R19}}
{{a|1R19}}
==1R19 Postmaintenance Testing==
==1R19 Postmaintenance Testing==
{{IP sample|IP=IP 71111.19}}
{{IP sample|IP=IP 71111.19}}
a. The inspectors reviewed the following postmaintenance activities to verify that procedures and test activities were adequate to ensure system operability and functional capability:
a.
Inspection Scope WO 00281193, "EGT
 
-TCV20B - Valve is Acting Irregularly (C R-11-4186)," reviewed on July 5, 2011 WO 52272756, "SWP
The inspectors reviewed the following postmaintenance activities to verify that procedures and test activities were adequate to ensure system operability and functional capability:
-AOV599 - Perform Functional Test of Standby Cooling Tower #1 Station," reviewed on July 6, 2011 WO 00284943, "GTS
Inspection Scope
-FLT1B During Performance of STP 0202 Discovered Low," reviewed on August 18, 2011 WO 00285929, "LSV
* WO 00281193, EGT-TCV20B - Valve is Acting Irregularly (CR-11-4186),reviewed on July 5, 2011
-C3B Water Leaking from LSV
* WO 52272756, SWP-AOV599 - Perform Functional Test of Standby Cooling Tower #1 Station, reviewed on July 6, 2011
-STR10BB While in Service," reviewed on August 21, 2011 WO 00275198, "Replace Relays ENB
* WO 00284943, GTS-FLT1B During Performance of STP-257-0202 Discovered Low, reviewed on August 18, 2011
-INV01B1," reviewed on September 21, 2011 WO 52249845, "1ENB*CHGR1B Load Test," reviewed on September 27, 2011 WO 00268148, "HVK-TS71D Calibration of Low Chill Water Temperature Pretrip," reviewed on September 29, 2011 The inspectors selected these activities based upon the structure, system, or component's ability to affect risk. The inspectors evaluated these activities for the following (as applicable):
* WO 00285929, LSV-C3B Water Leaking from LSV-STR10BB While in Service, reviewed on August 21, 2011
The effect of testing on the plant had been adequately addressed; testing was adequate for the maintenance performed Acceptance criteria were clear and demonstrated operational readiness; test instrumentation was appropriat e
* WO 00275198, Replace Relays ENB-INV01B1, reviewed on September 21, 2011
* WO 52249845, 1ENB*CHGR1B Load Test, reviewed on September 27, 2011
* WO 00268148, HVK-TS71D Calibration of Low Chill Water Temperature Pretrip, reviewed on September 29, 2011 The inspectors selected these activities based upon the structure, system, or component's ability to affect risk. The inspectors evaluated these activities for the following (as applicable):
* The effect of testing on the plant had been adequately addressed; testing was adequate for the maintenance performed
* Acceptance criteria were clear and demonstrated operational readiness; test instrumentation was appropriate
 
The inspectors evaluated the activities against the technical specifications, the Updated Safety Analysis Report, 10 CFR Part 50 requirements, licensee procedures, and various NRC generic communications to ensure that the test results adequately ensured that the equipment met the licensing basis and design requirements. In addition, the inspectors reviewed corrective action documents associated with postmaintenance tests to determine whether the licensee was identifying problems and entering them in the corrective action program and that the problems were being corrected commensurate with their importance to safety. Specific documents reviewed during this inspection are listed in the attachment.
The inspectors evaluated the activities against the technical specifications, the Updated Safety Analysis Report, 10 CFR Part 50 requirements, licensee procedures, and various NRC generic communications to ensure that the test results adequately ensured that the equipment met the licensing basis and design requirements. In addition, the inspectors reviewed corrective action documents associated with postmaintenance tests to determine whether the licensee was identifying problems and entering them in the corrective action program and that the problems were being corrected commensurate with their importance to safety. Specific documents reviewed during this inspection are listed in the attachment.


These activities constitute completion of seven postmaintenance testing inspection sample s as defined in Inspection Procedure
These activities constitute completion of seven postmaintenance testing inspection samples as defined in Inspection Procedure 71111.19-05.
 
==71111.19 - 05.==


b.
b.
Line 325: Line 369:
=====Introduction.=====
=====Introduction.=====
===
===
The inspectors identified a Green , noncited violation of 10 CFR Part 50, Appendix B, Criterion III, "Design Control," for an inadequate calculation methodology used in determining standby gas treatment system operability.
The inspectors identified a Green, noncited violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, for an inadequate calculation methodology used in determining standby gas treatment system operability.


Findings
Findings  


=====Description.=====
=====Description.=====
On July 21, 2011, the standby gas treatment filter train B heater failed the monthly surveillance test procedure due to an open electrical connection between a heater element and the mounting stud used to secure the element to the bus bar. The standby gas treatment systems filter train heaters have a total of nine heater elements, three elements per phase. Station engineering personnel developed engineering change EC-30850, "GTS-FLT1B Operation with One Heater Element out of Service," to temporarily remove the failed filter train heater element, and revised the surveillance test calculation method for determining filter train power output with only 8 out of 9 heater elements functioning. Technical Specification 5.5.7e , "Ventilation Filter Testing Program,"
On July 21, 2011, the standby gas treatment filter train B heater failed the monthly surveillance test procedure due to an open electrical connection between a heater element and the mounting stud used to secure the element to the bus bar.
requires that standby gas treatment system filter train B dissipate greater than or equal to 61 kW to maintain air relative humidity less than 70 percent passing through the filter
 
. On July 23, 2011, the filter train B passed the revised test procedure with very small margin, producing 61.43 kW. Humidity greater than 70 percent is considered detrimental to the charcoal filters ability to retain radioactive iodine.
The standby gas treatment systems filter train heaters have a total of nine heater elements, three elements per phase. Station engineering personnel developed engineering change EC-30850, GTS-FLT1B Operation with One Heater Element out of Service, to temporarily remove the failed filter train heater element, and revised the surveillance test calculation method for determining filter train power output with only 8 out of 9 heater elements functioning. Technical Specification 5.5.7e, Ventilation Filter Testing Program, requires that standby gas treatment system filter train B dissipate greater than or equal to 61 kW to maintain air relative humidity less than 70 percent passing through the filter. On July 23, 2011, the filter train B passed the revised test procedure with very small margin, producing 61.43 kW. Humidity greater than 70 percent is considered detrimental to the charcoal filters ability to retain radioactive iodine.


On August 17, 2011, the standby gas treatment filter train B heater failed the monthly surveillance test due to only producing 60.28 kW. Operations declared the system inoperable and actions were taken to repair the defective heater element. The system was returned to full qualification with nine heater elements installed, and passed the monthly surveillance.
On August 17, 2011, the standby gas treatment filter train B heater failed the monthly surveillance test due to only producing 60.28 kW. Operations declared the system inoperable and actions were taken to repair the defective heater element. The system was returned to full qualification with nine heater elements installed, and passed the monthly surveillance.


The inspectors reviewed the modified calculation methodology for standby gas treatment system heater operability. Neither the surveillance test nor engineering change EC-30850 calculation method accounted for instrument uncertainty when determining the kW output. The inspectors concluded that to have reasonable assurance of operability the calculation should have accounted for instrument uncertainty. The margin between the satisfactory test on July 23, 2011, and the unsatisfactory test on August 17, 2011, was within the instrument tolerances of the different amp and voltmeters used to measure the filter train heater current and voltage use. In addition, questioning by the inspectors revealed that the calculation had used a nonconservative value for the voltage drop from the heater breaker to the heater.
The inspectors reviewed the modified calculation methodology for standby gas treatment system heater operability. Neither the surveillance test nor engineering change EC-30850 calculation method accounted for instrument uncertainty when determining the kW output. The inspectors concluded that to have reasonable assurance of operability the calculation should have accounted for instrument uncertainty. The margin between the satisfactory test on July 23, 2011, and the  
 
unsatisfactory test on August 17, 2011, was within the instrument tolerances of the different amp and voltmeters used to measure the filter train heater current and voltage use. In addition, questioning by the inspectors revealed that the calculation had used a nonconservative value for the voltage drop from the heater breaker to the heater.


=====Analysis.=====
=====Analysis.=====
The failure to have an adequate calculation methodology for the standby gas treatment heater output power is a performance deficiency. The inspectors determined that the performance deficiency was similar to the "not minor if" statement contained in example 3j of Inspection Manual Chapter 0612, Appendix E, "Examples of Minor Issues," because reasonable doubt of system operability existed. Using Inspection Manual Chapter 0612, Appendix B, "Issue Screening," the inspectors determined that this finding was more than minor because it was associated with the design control attribute of the Barrier Integrity Cornerstone to maintain radiological barrier functionality of standby gas treatment trains , and affected the cornerstone objective to provide reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents or events.
The failure to have an adequate calculation methodology for the standby gas treatment heater output power is a performance deficiency. The inspectors determined that the performance deficiency was similar to the not minor if statement contained in example 3j of Inspection Manual Chapter 0612, Appendix E, Examples of Minor Issues, because reasonable doubt of system operability existed. Using Inspection Manual Chapter 0612, Appendix B, Issue Screening, the inspectors determined that this finding was more than minor because it was associated with the design control attribute of the Barrier Integrity Cornerstone to maintain radiological barrier functionality of standby gas treatment trains, and affected the cornerstone objective to provide reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents or events. Specifically, operating the standby gas system filter train heaters without sufficient output power is detrimental to the ability of the charcoal filters to retain radioactive iodine. This could result in a greater amount of radiation release to the environment in the event of an accident. In accordance with Inspection manual Chapter 0609, Appendix A, Significance Determination of Reactor Inspection Findings for At-Power Situations, the Phase 1 significance determination process screening determined the finding to be only of very low safety significance (Green) because the finding only represented a degradation of the radiological barrier function provided for the standby gas treatment system. The apparent cause of this finding was the decision to develop an engineering evaluation that did not include instrument uncertainly and did not validate the correct voltage drop between the filter train heater feeder breaker and the heater elements. The cause of this finding has a crosscutting aspect in the area of human performance associated with the decision-making component because station personnel failed to use conservative assumptions when developing the modified output power methodology for operation of the standby gas treatment system filter heaters with only 8 of 9 heater elements installed [H.1(b)].  


Specifically, operating the standby gas system filter train heaters without sufficient output power is detrimental to the ability of the charcoal filters to retain radioactive iodine. This could result in a greater amount of radiation release to the environment in the event of an accident. In accordance with Inspection manual Chapter 0609, Appendix A, "Significance Determination of Reactor Inspection Findings for At
=====Enforcement.=====
-Power Situations," the Phase 1 significance determination process screening determined the finding to be only of very low safety significance (Green) because the finding only represented a degradation of the radiological barrier function provided for the standby gas treatment system. The apparent cause of this finding was the decision to develop an engineering evaluation that did not include instrument uncertainly and did not validate the correct voltage drop between the filter train heater feeder breaker and the heater elements.
Title 10 CFR Part 50, Appendix B, Criterion III, Design Control requires, in part, that design control measures provide for verifying or checking the adequacy of design, such as by the performance of design reviews, by the use of alternate or simplified calculational methods, or by the performance of suitable testing program.


The cause of this finding has a crosscutting aspect in the area of human performance associated with the decision
Contrary to this, on July 23, 2011, the licensees design control measures did not provide for verifying the adequacy of design, in that those measures failed to verify satisfactory performance of the standby gas treatment system due to the failure of station personnel to account for instrument uncertainty in the modified heater output calculation. Because this finding was of very low safety significance and has been entered into the licensees corrective action program as Condition Report CR-RBS-2100-07332, this violation is being treated as a noncited violation consistent with NRC Enforcement Policy: NCV 05000458/2011004-01, Inadequate Standby Gas Treatment Electric Heater Power Output Calculation.
-making component because station personnel failed to use conservative assumptions when developing the modified output power methodology for operation of the standby gas treatment system filter heaters with only 8 of 9 heater elements installed [H.1(b)].
{{a|1R22}}


=====Enforcement.=====
==1R22 Surveillance Testing==
Title 10 CFR Part 50, Appendix B, Criterion III, "Design Control" requires, in part, that design control measures provide for verifying or checking the adequacy of design, such as by the performance of design reviews, by the use of alternate or simplified calculational methods, or by the performance of suitable testing program. Contrary to this, on July 23, 2011, the licensee's design control measures did not provide for verifying the adequacy of design, in that those measures failed to verify satisfactory performance of the standby gas treatment system due to the failure of station personnel to account for instrument uncertainty in the modified heater output calculation. Because this finding was of very low safety significance and has been entered into the licensee's corrective action program as Condition Report CR-RBS-2100-07332, this violation is being treated as a noncited violation consistent with NRC Enforcement Policy:
NCV 05000458/2011004
-01, "Inadequate Standby Gas Treatment Electric Heater Power Output Calculation."
{{a|R22}}
==R22 Surveillance Testing==
{{IP sample|IP=IP 71111.22}}
{{IP sample|IP=IP 71111.22}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the Updated Safety Analysis Report, procedure requirements, and technical specifications to ensure that the surveillance activities listed below demonstrated that the systems, structures, and/or components tested were capable of performing their intended safety functions. The inspectors either witnessed or reviewed test data to verify that the significant surveillance test attributes were adequate to address the following:
The inspectors reviewed the Updated Safety Analysis Report, procedure requirements, and technical specifications to ensure that the surveillance activities listed below demonstrated that the systems, structures, and/or components tested were capable of performing their intended safety functions. The inspectors either witnessed or reviewed test data to verify that the significant surveillance test attributes were adequate to address the following:
Preconditioning
* Preconditioning
* Evaluation of testing impact on the plant
* Acceptance criteria
* Test equipment
* Procedures
* Jumper/lifted lead controls
* Test data
* Testing frequency and method demonstrated technical specification operability
* Test equipment removal
* Restoration of plant systems
* Fulfillment of ASME Code requirements
* Updating of performance indicator data
* Engineering evaluations, root causes, and bases for returning tested systems, structures, and components not meeting the test acceptance criteria were correct
* Reference setting data
* Annunciators and alarms setpoints


Evaluation of testing impact on the plant
The inspectors also verified that licensee personnel identified and implemented any needed corrective actions associated with the surveillance testing.
* STP-204-6301, DIV I LPCI (RHR) Pump and Valve Operability Test, performed inservice test sample on July 7, 2011
* STP-257-4501, RMS Primary Containment Purge Isolation Radiation High Activity Monitor Channel Functional Test (RMS-RE21A), on July 10, 2011
* STP-309-0603, Division III ECCS Test, performed on July 26, 2011
* REP-0007, Spent Fuel Pool Coupon Surveillance Program, performed on August 22, 2011
* STP-204-4510, LPCI Pump C Discharge Flow - Low, Channel Functional Test (E12-N652C), performed on September 13, 2011 Specific documents reviewed during this inspection are listed in the attachment.


Acceptance criteria
These activities constitute completion of five surveillance testing inspection samples as defined in Inspection Procedure 71111.22-05.


Test equipment
b.


Procedures
No findings were identified.


Jumper/lifted lead controls
Findings
{{a|1EP6}}


Test data Testing frequency and method demonstrated technical specification operability
==1EP6 Drill Evaluation==
{{IP sample|IP=IP 71114.06}}
Emergency Preparedness Drill Observation a.


Test equipment removal
The inspectors evaluated the conduct of routine licensee emergency drills on July 14, 2011, and August 2, 2011, to identify any weaknesses and deficiencies in classification, notification, and protective action recommendation development activities.


Restoration of plant systems
The inspectors observed emergency response operations in the simulator, emergency operations facility, and technical support center to determine whether the event classification, notifications, and protective action recommendations were performed in accordance with procedures. The inspectors also attended the licensee drill critique to compare any inspector-observed weakness with those identified by the licensee staff in order to evaluate the critique and to verify whether the licensee staff was properly identifying weaknesses and entering them into the corrective action program. As part of the inspection, the inspectors reviewed the drill package and other documents listed in the attachment.


Fulfillment of ASME Code requirements
Inspection Scope


Updating of performance indicator data
These activities constitute completion of two samples as defined in Inspection Procedure 71114.06-05.


Engineering evaluations, root causes, and bases for returning tested systems, structures, and components not meeting the test acceptance criteria were correct Reference setting data Annunciators and alarms setpoints The inspectors also verified that licensee personnel identified and implemented any needed corrective actions associated with the surveillance testing.
b.


STP-204-6301 , "DIV I LPCI (RHR) Pump and Valve Operability Test," performed inservice test sample on July 7, 2011 STP-257-4501 , "RMS Primary Containment Purge Isolation Radiation High Activity Monitor Channel Functional Test (RMS
No findings were identified.
-RE21A)," on July 10, 2011 STP-309-0603, "Division III ECCS Test," performed on July 26, 2011 REP-0007, "Spent Fuel Pool Coupon Surveillance Program," performed on August 22, 2011 STP-204-4510, "LPCI Pump C Discharge Flow
- Low, Channel Functional Test (E12-N652C)," performed on September 13, 2011 Specific documents reviewed during this inspection are listed in the attachment.
 
These activities constitute completion of five surveillance testing inspection sample s as defined in Inspection Procedure
 
==71111.22 - 05.==
b. No findings were identified.


Findings
Findings
{{a|1EP6}}
==1EP6 Drill Evaluation==
{{IP sample|IP=IP 71114.06}}
Emergency Preparedness Drill Observation a. The inspectors evaluated the conduct of routine licensee emergency drill s on July 14, 2011, and August 2, 2011, to identify any weaknesses and deficiencies in classification, notification, and protective action recommendation development activities. The inspectors observed emergency response operations in the simulator, emergency operations facility, and technical support center to determine whether the event classification, notifications, and protective action recommendations were performed in accordance with procedures. The inspectors also attended the licensee drill critique to compare any inspector
-observed weakness with those identified by the licensee staff in order to evaluate the critique and to verify whether the licensee staff was properly identifying weaknesses and entering them into the corrective action program. As part of the inspection, the inspectors reviewed the drill package and other documents listed in the attachment.
Inspection Scope These activities constitute completion of two samples as defined in Inspection Procedure
==71114.06 - 05.==
b. No findings were identified.
Findings 


==RADIATION SAFETY==
==RADIATION SAFETY==
===Cornerstone: Occupational and Public Radiation Safety===
{{a|2RS0}}


===Cornerstone:===
Occupational and Public Radiation Safety
{{a|2RS0}}
==2RS0 6 Radioactive Gaseous and Liquid Effluent Treatment==
==2RS0 6 Radioactive Gaseous and Liquid Effluent Treatment==
{{IP sample|IP=IP 71124.06}}
{{IP sample|IP=IP 71124.06}}


====a. Inspection Scope====
====a. Inspection Scope====
This area was inspected to: (1)ensure the gaseous and liquid effluent processing systems are maintained so radiological discharges are properly mitigated, monitored, and evaluated with respect to public exposure;
This area was inspected to:
: (2) ensure abnormal radioactive gaseous or liquid discharges and conditions, when effluent radiation monitors are out
: (1) ensure the gaseous and liquid effluent processing systems are maintained so radiological discharges are properly mitigated, monitored, and evaluated with respect to public exposure;
-of-service, are controlled in accordance with the applicable regulatory requirements and licensee procedures;
: (2) ensure abnormal radioactive gaseous or liquid discharges and conditions, when effluent radiation monitors are out-of-service, are controlled in accordance with the applicable regulatory requirements and licensee procedures;
: (3) verify the licensee
: (3) verify the licensee=s quality control program ensures the radioactive effluent sampling and analysis requirements are satisfied so discharges of radioactive materials are adequately quantified and evaluated; and
=s quality control program ensures the radioactive effluent sampling and analysis requirements are satisfied so discharges of radioactive materials are adequately quantified and evaluated; and
: (4) verify the adequacy of public dose projections resulting from radioactive effluent discharges. The inspectors used the requirements in 10 CFR Part 20; 10 CFR Part 50, Appendices A and I; 40 CFR Part 190; the Offsite Dose Calculation Manual, and licensee procedures required by the Technical Specifications as criteria for determining compliance. The inspectors interviewed licensee personnel and reviewed and/or observed the following items:
: (4) verify the adequacy of public dose projections resulting from radioactive effluent discharges. The inspectors used the requirements in 10 CFR Part 20; 10 CFR Part 50, Appendices A and I; 40 CFR Part 190; the Offsite Dose Calculation Manual, and licensee procedures required by the Technical Specifications as criteria for determining compliance. The inspectors interviewed licensee personnel and reviewed and/or observed the following items:
Radiological effluent release reports since the previous inspection and reports related to the effluent program issued since the previous inspection, if any Effluent program implementing procedures, including sampling, monitor setpoint determinations and dose calculations Equipment configuration and flow paths of selected gaseous and liquid discharge system components, filtered ventilation system material condition, and significant changes to their effluent release points, if any, and associated 10 CFR 50.59 reviews   Selected portions of the routine processing and discharge of radioactive gaseous and liquid effluent s (including sample collection and analysis)
* Radiological effluent release reports since the previous inspection and reports related to the effluent program issued since the previous inspection, if any
Controls used to ensure representative sampling and appropriate compensatory sampling   Results of the inter
* Effluent program implementing procedures, including sampling, monitor setpoint determinations and dose calculations
-laboratory comparison program Effluent stack flow rates Surveillance test results of technical specification
* Equipment configuration and flow paths of selected gaseous and liquid discharge system components, filtered ventilation system material condition, and significant changes to their effluent release points, if any, and associated 10 CFR 50.59 reviews
-required ventilation effluent discharge systems since the previous inspection   Significant changes in reported dose values, if any A selection of radioactive liquid and gaseous waste discharge permits Part 61 analyses and methods used to determine which isotopes are included in the source term Offsite dose calculation manual changes, if any Meteorological dispersion and deposition factors Latest land use censu s    Records of abnormal gaseous or liquid tank discharges, if any Groundwater monitoring results Changes to the licensee
* Selected portions of the routine processing and discharge of radioactive gaseous and liquid effluents (including sample collection and analysis)
's written program for indentifying and controlling contaminated spills/leaks to groundwater, if any Identified leakage or spill events and entries made into 10 CFR 50.75
* Controls used to ensure representative sampling and appropriate compensatory sampling
: (g) records, if any, and associated evaluations of the extent of the contamination and the radiological source term Offsite notifications and reports of events associated with spills, leaks, or groundwater monitoring results, if any   Audits, self
* Results of the inter-laboratory comparison program
-assessments, reports, and corrective action documents related to radioactive gaseous and liquid effluent treatment since the last inspection Specific documents reviewed during this inspection are listed in the attachment.
* Effluent stack flow rates
* Surveillance test results of technical specification-required ventilation effluent discharge systems since the previous inspection
* Significant changes in reported dose values, if any
* A selection of radioactive liquid and gaseous waste discharge permits
* Part 61 analyses and methods used to determine which isotopes are included in the source term
* Offsite dose calculation manual changes, if any
* Meteorological dispersion and deposition factors
* Latest land use census
* Records of abnormal gaseous or liquid tank discharges, if any
* Groundwater monitoring results
* Changes to the licensees written program for indentifying and controlling contaminated spills/leaks to groundwater, if any
* Identified leakage or spill events and entries made into 10 CFR 50.75 (g)records, if any, and associated evaluations of the extent of the contamination and the radiological source term
* Offsite notifications and reports of events associated with spills, leaks, or groundwater monitoring results, if any
* Audits, self-assessments, reports, and corrective action documents related to radioactive gaseous and liquid effluent treatment since the last inspection  
 
Specific documents reviewed during this inspection are listed in the attachment.


These activities constitute completion of the one required sample , as defined in Inspection Procedure 7112 4.0 6-05.
These activities constitute completion of the one required sample, as defined in Inspection Procedure 71124.06-05.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|2RS0}}
{{a|2RS0}}
 
==2RS0 7 Radiological Environmental Monitoring Program==
==2RS0 7 Radiological Environmental Monitoring Program==
{{IP sample|IP=IP 71124.07}}
{{IP sample|IP=IP 71124.07}}
Line 438: Line 495:
This area was inspected to:
This area was inspected to:
: (1) ensure that the radiological environmental monitoring program verifies the impact of radioactive effluent releases to the environment and sufficiently validates the integrity of the radioactive gaseous and liquid effluent release program;
: (1) ensure that the radiological environmental monitoring program verifies the impact of radioactive effluent releases to the environment and sufficiently validates the integrity of the radioactive gaseous and liquid effluent release program;
: (2) verify that the radiological environmental monitoring program is implemented consistent with the licensee's technical specifications and/or offsite dose calculation manual, and to validate that the radioactive effl uent release program meets the design objective contained in Appendix I to 10 CFR Part 50; and
: (2) verify that the radiological environmental monitoring program is implemented consistent with the licensees technical specifications and/or offsite dose  
: (3) ensure that the radiological environmental monitoring program monitors non
-effluent exposure pathways, is based on sound principles and assumptions, and validates that doses to members of the public are within the dose limits of 10 CFR Part 20 and 40 CFR Part 190 , as applicable. The inspectors reviewed and/or observed the following items:  Annual environmental monitoring reports and offsite dose calculation manual Selected air sampling and thermoluminescence dosimeter monitoring stations Collection and preparation of environmental samples


Operability, calibration, and maintenance of meteorological instruments Selected event s documented in the annual environmental monitoring report which involved a missed sample, inoperable sampler, lost thermoluminescence dosimeter, or anomalous measurement Selected structures, systems, or components that may contain licensed material and has a credible mechanism for licensed material to reach ground water Records required by 10 CFR 50.75(g)
calculation manual, and to validate that the radioactive effluent release program meets the design objective contained in Appendix I to 10 CFR Part 50; and
Significant changes made by the licensee to the offsite dose calculation manual as the result of changes to the land census or sampler station modifications since the last inspection Calibration and maintenance records for selected air samplers, composite water samplers, and environmental sample radiation measurement instrumentation Interlaboratory comparison program results Audits, self
: (3) ensure that the radiological environmental monitoring program monitors non-effluent exposure pathways, is based on sound principles and assumptions, and validates that doses to members of the public are within the dose limits of 10 CFR Part 20 and 40 CFR Part 190, as applicable. The inspectors reviewed and/or observed the following items:
-assessments, reports, and corrective action documents related to the radiological environmental monitoring program since the last inspection Specific documents reviewed during this inspection are listed in the attachment.
* Annual environmental monitoring reports and offsite dose calculation manual
* Selected air sampling and thermoluminescence dosimeter monitoring stations
* Collection and preparation of environmental samples
* Operability, calibration, and maintenance of meteorological instruments
* Selected events documented in the annual environmental monitoring report which involved a missed sample, inoperable sampler, lost thermoluminescence dosimeter, or anomalous measurement
* Selected structures, systems, or components that may contain licensed material and has a credible mechanism for licensed material to reach ground water
* Records required by 10 CFR 50.75(g)
* Significant changes made by the licensee to the offsite dose calculation manual as the result of changes to the land census or sampler station modifications since the last inspection
* Calibration and maintenance records for selected air samplers, composite water samplers, and environmental sample radiation measurement instrumentation
* Interlaboratory comparison program results
* Audits, self-assessments, reports, and corrective action documents related to the radiological environmental monitoring program since the last inspection  
 
Specific documents reviewed during this inspection are listed in the attachment.


These activities constitute completion of the one required sample as defined in Inspection Procedure 71124.0 7-05.
These activities constitute completion of the one required sample as defined in Inspection Procedure 71124.07-05.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.


RS08 Radioactive Solid Waste Processing, and Radioactive Material Handling, Storage, and Transportation (71124.08)
2RS08 Radioactive Solid Waste Processing, and Radioactive Material Handling, Storage, and Transportation (71124.08)


====a. Inspection Scope====
====a. Inspection Scope====
This area was inspected to verify the effectiveness of the licensee
This area was inspected to verify the effectiveness of the licensee=s programs for processing, handling, storage, and transportation of radioactive material. The inspectors used the requirements of 10 CFR Parts 20, 61, and 71 and Department of Transportation regulations contained in 49 CFR Parts 171-180 for determining compliance. The inspectors interviewed licensee personnel and reviewed the following items:
=s programs for processing, handling, storage, and transportation of radioactive material. The inspectors used the requirements of 10 CFR Parts 20, 61, and 71 and Department of Transportation regulations contained in 49 CFR Parts 171-180 for determining compliance. The inspectors interviewed licensee personnel and reviewed the following items:   The solid radioactive waste system description, process control program, and the scope of the licensee
* The solid radioactive waste system description, process control program, and the scope of the licensee=s audit program
=s audit program Control of radioactive waste storage areas including container labeling/marking and monitoring containers for deformation or signs of waste decomposition Changes to the liquid and solid waste processing system configuration including a review of waste processing equipment that is not operational or abandoned in place   Radio-chemical sample analysis results for radioactive waste streams and use of scaling factors and calculations to account for difficult
* Control of radioactive waste storage areas including container labeling/marking and monitoring containers for deformation or signs of waste decomposition
-to-measure radionuclides  
* Changes to the liquid and solid waste processing system configuration including a review of waste processing equipment that is not operational or abandoned in place
* Radio-chemical sample analysis results for radioactive waste streams and use of scaling factors and calculations to account for difficult-to-measure radionuclides
* Processes for waste classification including use of scaling factors and 10 CFR Part 61 analysis
* Shipment packaging, surveying, labeling, marking, placarding, vehicle checking, driver instructing, and preparation of the disposal manifest
* Audits, self-assessments, reports, and corrective action reports radioactive solid waste processing, and radioactive material handling, storage, and transportation performed since the last inspection


Processes for waste classification including use of scaling factors and 10 CFR Part 61 analysis Shipment packaging, surveying, labeling, marking, placarding, vehicle checking, driver instructing, and preparation of the disposal manifest Audits, self
Specific documents reviewed during this inspection are listed in the attachment.
-assessments, reports, and corrective action reports radioactive solid waste processing, and radioactive material handling, storage, and transportation performed since the last inspection Specific documents reviewed during this inspection are listed in the attachment.


These activities constitute completion of the one required sample as defined in Inspection Procedure
These activities constitute completion of the one required sample as defined in Inspection Procedure 71124.08-05.
 
==71124.08 - 05.==


====b. Findings====
====b. Findings====
Line 471: Line 539:
==OTHER ACTIVITIES==
==OTHER ACTIVITIES==
{{a|4OA1}}
{{a|4OA1}}
==4OA1 Performance Indicator Verification==
==4OA1 Performance Indicator Verification==
{{IP sample|IP=IP 71151}}
{{IP sample|IP=IP 71151}}
===.1 Data Submission Issue===
===.1 Data Submission Issue===
a.


a. The inspectors performed a review of the performance indicator data submitted by the licensee for the second quarter 2011 performance indicators for any obvious inconsistencies prior to its public release in accordance with Inspection Manual Chapter 0608, "Performance Indicator Program."
The inspectors performed a review of the performance indicator data submitted by the licensee for the second quarter 2011 performance indicators for any obvious inconsistencies prior to its public release in accordance with Inspection Manual Chapter 0608, Performance Indicator Program.


Inspection Scope This review was performed as part of the inspectors' normal plant status activities and, as such, did not constitute a separate inspection sample.
Inspection Scope  


b. No findings were identified.
This review was performed as part of the inspectors normal plant status activities and, as such, did not constitute a separate inspection sample.
 
b.
 
No findings were identified.


Findings
Findings


===.2 Mitigating Systems Performance Index===
===.2 Mitigating Systems Performance Index - Heat Removal System (MS08)===
a.
 
The inspectors sampled licensee submittals for the mitigating systems performance index - heat removal system performance indicator for the period from the third quarter 2010 through the second quarter 2011. To determine the accuracy of the performance indicator data reported during those periods, the inspectors used definitions and guidance contained in NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6. The inspectors reviewed the licensees operator narrative logs, issue reports, event reports, mitigating systems performance index derivation reports, and NRC integrated inspection reports for the period of July 2010 through June 2011 to validate the accuracy of the submittals. The inspectors reviewed the mitigating systems performance index component risk coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the performance indicator data collected or transmitted for this indicator and none were identified. Specific documents reviewed are described in the attachment to this report.
 
Inspection Scope


- Heat Removal System (MS08)a. The inspectors sampled licensee submittals for the mitigating systems performance index - heat removal system performance indicator for the period from the third quarter 2010 through the second quarter 2011. To determine the accuracy of the performance indicator data reported during those periods, the inspectors used definitions and guidance contained in NEI Document 99
These activities constitute completion of one mitigating systems performance index - heat removal system sample as defined in Inspection Procedure 71151-05.
-02, "Regulatory Assessment Performance Indicator Guideline," Revision 6. The inspectors reviewed the licensee's operator narrative logs, issue reports, event reports, mitigating systems performance index derivation reports, and NRC integrated inspection reports for the period of July 2010 through June 2011 to validate the accuracy of the submittals. The inspectors reviewed the mitigating systems performance index component risk coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensee's issue report database to determine if any problems had been identified with the performance indicator data collected or transmitted for this indicator and none were identified. Specific documents reviewed are described in the attachment to this report.


Inspection Scope
b.


These activities constitute completion of one mitigating systems performance index
No findings were identified.
- heat removal system sample as defined in Inspection Procedure 71151-05. b. No findings were identified.


Findings
Findings


===.3 Mitigating Systems Performance Index===
===.3 Mitigating Systems Performance Index - Residual Heat Removal System (MS09)===
a.
 
The inspectors sampled licensee submittals for the mitigating systems performance index - residual heat removal system performance indicator for the period from the third quarter 2010 through the second quarter 2011. To determine the accuracy of the performance indicator data reported during those periods, the inspectors used definitions and guidance contained in NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6. The inspectors reviewed the licensees operator narrative logs, issue reports, mitigating systems performance index derivation reports, event reports, and NRC integrated inspection reports for the period of July 2010 through June 2011 to validate the accuracy of the submittals. The inspectors reviewed the mitigating systems performance index component risk coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the performance indicator data collected or transmitted for this indicator and none were identified. Specific documents reviewed are described in the attachment to this report.
 
Inspection Scope


- Residual Heat Removal System (MS09)a. The inspectors sampled licensee submittals for the mitigating systems performance index - residual heat removal system performance indicator for the period from the third quarter 2010 through the second quarter 2011. To determine the accuracy of the performance indicator data reported during those periods, the inspectors used definitions and guidance contained in NEI Document 99
These activities constitute completion of one mitigating systems performance index - residual heat removal system sample as defined in Inspection Procedure 71151-05.
-02, "Regulatory Assessment Performance Indicator Guideline," Revision 6. The inspectors reviewed the licensee's operator narrative logs, issue reports, mitigating systems performance index derivation reports, event reports, and NRC integrated inspection reports for the period of July 2010 through June 2011 to validate the accuracy of the submittals. The inspectors reviewed the mitigating systems performance index component risk coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensee's issue report database to determine if any problems had been identified with the performance indicator data collected or transmitted for this indicator and none were identified. Specific documents reviewed are described in the attachment to this report.


Inspection Scope These activities constitute completion of one mitigating systems performance index
b.
- residual heat removal system sample as defined in Inspection Procedure 71151-05. b. No findings were identified.
 
No findings were identified.


Findings
Findings


===.4 Mitigating Systems Performance Index===
===.4 Mitigating Systems Performance Index - Cooling Water Systems (MS10)===
a.


- Cooling Water Systems (MS10)a. The inspectors sampled licensee submittals for the mitigating systems performance index - cooling water systems performance indicator for the period from the third quarter 2010 through the second quarter 2011. To determine the accuracy of the performance indicator data reported during those periods, the inspectors used definitions and guidance contained in NEI Document 99
The inspectors sampled licensee submittals for the mitigating systems performance index - cooling water systems performance indicator for the period from the third quarter 2010 through the second quarter 2011. To determine the accuracy of the performance indicator data reported during those periods, the inspectors used definitions and guidance contained in NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6. The inspectors reviewed the licensees operator narrative logs, issue reports, mitigating systems performance index derivation reports, event reports, and NRC integrated inspection reports for the period of July 2010 through June 2011 to validate the accuracy of the submittals. The inspectors reviewed the mitigating systems performance index component risk coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the performance indicator data collected or transmitted for this indicator and none were identified. Specific documents reviewed are described in the attachment to this report.
-02, "Regulatory Assessment Performance Indicator Guideline," Revision 6. The inspectors reviewed the licensee's operator narrative logs, issue reports, mitigating systems performance index derivation reports, event reports, and NRC integrated inspection reports for the period of July 2010 through June 2011 to validate the accuracy of the submittals. The inspectors reviewed the mitigating systems performance index component risk coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensee's issue report database to determine if any problems had been identified with the performance indicator data collected or transmitted for this indicator and none were identified. Specific documents reviewed are described in the attachment to this report.


Inspection Scope These activities constitute completion of one mitigating systems performance index  
Inspection Scope  
- cooling water system sample as defined in Inspection Procedure 71151-05. b. No findings were identified.
 
These activities constitute completion of one mitigating systems performance index - cooling water system sample as defined in Inspection Procedure 71151-05.
 
b.
 
No findings were identified.


Findings
Findings
{{a|4OA2}}
{{a|4OA2}}
==4OA2 Identification and Resolution of Problems==
==4OA2 Identification and Resolution of Problems==
{{IP sample|IP=IP 71152}}
{{IP sample|IP=IP 71152}}
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical Protection
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical Protection


===.1 Routine Review of Identification and Resolution of Problems===
===.1 Routine Review of Identification and Resolution of Problems===
a.


a. As part of the various baseline inspection procedures discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that they were being entered into the licensee's corrective action program at an appropriate threshold, that adequate attention was being given to timely corrective actions, and that adverse trends were identified and addressed. The inspectors reviewed attributes that included the complete and accurate identification of the problem; the timely correction, commensurate with the safety significance; the evaluation and disposition of performance issues, generic implications, common causes, contributing factors, root causes, extent of condition reviews, and previous occurrences reviews; and the classification, prioritization, focus, and timeliness of corrective actions. Minor issues entered into the licensee's corrective action program because of the inspectors' observations are included in the attached list of documents reviewed. Inspection Scope These routine reviews for the identification and resolution of problems did not constitute any additional inspection samples. Instead, by procedure, they were considered an integral part of the inspections performed during the quarter and documented in Section 1 of this report.
As part of the various baseline inspection procedures discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that they were being entered into the licensees corrective action program at an appropriate threshold, that adequate attention was being given to timely corrective actions, and that adverse trends were identified and addressed. The inspectors reviewed attributes that included the complete and accurate identification of the problem; the timely correction, commensurate with the safety significance; the evaluation and disposition of performance issues, generic implications, common causes, contributing factors, root causes, extent of condition reviews, and previous occurrences reviews; and the classification, prioritization, focus, and timeliness of corrective actions. Minor issues entered into the licensees corrective action program because of the inspectors observations are included in the attached list of documents reviewed.


b. No findings were identified.
Inspection Scope
 
These routine reviews for the identification and resolution of problems did not constitute any additional inspection samples. Instead, by procedure, they were considered an integral part of the inspections performed during the quarter and documented in Section 1 of this report.
 
b.
 
No findings were identified.


Findings
Findings


===.2 Daily Corrective Action Program Reviews===
===.2 Daily Corrective Action Program Reviews===
a.
In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of Inspection Scope
items entered into the licensees corrective action program. The inspectors accomplished this through review of the stations daily corrective action documents.
The inspectors performed these daily reviews as part of their daily plant status monitoring activities and, as such, did not constitute any separate inspection samples.


a. In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow
b.
-up, the inspectors performed a daily screening of Inspection Scope items entered into the licensee's corrective action program. The inspectors accomplished this through review of the station's daily corrective action documents.


The inspectors performed these daily reviews as part of their daily plant status monitoring activities and, as such, did not constitute any separate inspection samples. b. No findings were identified.
No findings were identified.


Findings
Findings


===.3 Selected Issue Follow===
===.3 Selected Issue Follow-up Inspection===
a.
 
During a review of items entered in the licensees corrective action program, the inspectors recognized a corrective action item documenting an event involving a downpower due to a steam leak on a main steam equalizing header drain. The inspectors discussed the event with licensee management, engineering, operations, and maintenance personnel to understand the event and the scope of the corrective actions taken by the licensee.


-up Inspection a. During a review of items entered in the licensee's corrective action program, the inspectors recognized a corrective action item documenting an event involving a downpower due to a steam leak on a main steam equalizing header drain. The inspectors discussed the even t with licensee management, engineering, operations, and maintenance personnel to understand the event and the scope of the corrective actions taken by the licensee.
Inspection Scope


Inspection Scope These activities constitute completion of one in-depth problem identification and resolution sample as defined in Inspection Procedure
These activities constitute completion of one in-depth problem identification and resolution sample as defined in Inspection Procedure 71152-05.


==71152 - 05.==
b.
b.


=====Introduction.=====
=====Introduction.=====
The inspectors identified a self
The inspectors identified a self-revealing, Green finding involving inadequate corrective actions in response to a failure in the main steam equalizing header drain bypass valve, resulting in a steam leak and an unplanned plant down power.
-revealing, Green finding involving inadequate corrective actions in response to a failure in the main steam equalizing header drain bypass valve, resulting in a steam leak and an unplanned plant down power. Findings
 
Findings  


=====Description.=====
=====Description.=====
On February 12, 2011, during plant start
On February 12, 2011, during plant start-up from refuel outage 16, plant operators discovered that the main steam equalizing header drain bypass valve had dual position indication instead of closed. This information was reported to the outage control center. Based on previous maintenance during the outage and operation of the valve earlier in the plant start-up, the outage control center and main control room personnel presumed the dual position indication was an indication only issue and the actual valve position was closed as intended. Station management failed to take adequate follow-up actions to ensure the valve was in the closed position, and also failed to address the potential consequences of normal power operations with the valve partially open.
-up from refuel outage 16, plant operators discovered that the main steam equalizing header drain bypass valve had dual position indication instead of closed.


This information was reported to the outage control center. Based on previous maintenance during the outage and operation of the valve earlier in the plant start
On June 19, 2011, plant operators in the turbine building identified a large steam leak near the condenser. Operators reduced station power to approximately 40 percent in order to facilitate identification of the leak. During the investigation, station personnel found that the main steam equalizing header drain piping developed a through wall leak beyond the bypass valve. The valve had not been in the closed position and was partially open. Consequently, fluid flow through the valve increased, causing water to
-up, the outage control center and main control room personnel presumed the dual position indication was an "indication only" issue and the actual valve position was closed as intended.


Station management failed to take adequate follow-up actions to ensure the valve was in the closed position, and also failed to address the potential consequences of normal power operations with the valve partially open.
flash to steam due to the large pressure drop near the condenser resulting in accelerated pipe wall erosion and piping failure. Station personnel isolated the damaged steam drain piping and returned the plant to full power.


On June 19, 2011, plant operators in the turbine building identified a large steam leak near the condenser. Operators reduced station power to approximately 40 percent in order to facilitate identification of the leak. During the investigation, station personnel found that the main steam equalizing header drain piping developed a through wall leak beyond the bypass valve.
Corrective actions included plans to develop and implement a comprehensive program that establishes nuclear safety culture as the overriding station priority; perform a needs analysis to determine training requirements related to the importance of aggressively pursuing the satisfactory resolution of abnormal conditions (e.g., this condition where a valve dual position indication was not verified by other means as correct); troubleshoot the valve during refueling outage 17 to determine why the valve failed to close; evaluate the piping failure mechanism to incorporate the findings into flow accelerated corrosion program as needed; and replace any damage piping during refueling outage 17.


The valve had not been in the closed position and was partially open. Consequently, fluid flow through the valve increased , causing water to flash to steam due to the large pressure drop near the condenser resulting in accelerated pipe wall erosion and piping failure
=====Analysis.=====
. Station personnel isolated the damaged steam drain piping and returned the plant to full power.
The failure to ensure that the corrective action process properly addressed the dual indication on the bypass valve during plant start-up was a performance deficiency.


Corrective actions include d plans to develop and implement a comprehensive program that establishes nuclear safety culture as the overriding station priority; perform a needs analysis to determine training requirements related to the importance of aggressively pursuing the satisfactory resolution of abnormal conditions (e.g., this condition where a valve dual position indication was not verified by other means as correct); troubleshoot the valve during refueling outage 17 to determine why the valve failed to close; evaluate the piping failure mechanism to incorporate the findings into flow accelerated corrosion program as needed; and replace any damage piping during refueling outage 17.
Specifically, EN-LI-102, "Corrective Action Process," states that individuals are required to take immediate actions to resolve adverse conditions to minimize the consequence of the condition. Contrary to this, during refuelling outage 16, the outage control center and main control room personnel failed to adequately investigate the dual indications identified on the main steam equalizing header drain bypass valve. The finding was more than minor because it was associated with the equipment performance attribute of the initiating events cornerstone and affected the cornerstone objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. The inspectors reviewed the finding using Inspection Manual Chapter 0609, Appendix A, Significance Determination of Reactor Inspection Findings for At-Power Situations. Based on the Phase 1 screening of the finding, the inspectors determined that the finding was of very low safety significance (Green) because it was not a loss of coolant accident initiator, did not contribute to both the likelihood of an initiating event and the likelihood that mitigating equipment or functions would not be available, nor increase the likelihood of an external event (seismic, flooding, or severe weather event). The apparent cause of the performance deficiency was that the control room and outage control center personnel presumed that the main control room dual indication for the valve was incorrect because previously valve operation successfully closed the valve. Consequently, this finding has a crosscutting aspect in the area of human performance associated with the decision-making component because station personnel failed to use a systematic process to assess the condition of the bypass valve, and failed to verify the validity of the underlying assumptions that were used to justify operation with the valve having dual indication
[H.1(a)].  


=====Analysis.=====
=====Enforcement.=====
The failure to ensure that the corrective action process properly addressed the dual indication on the bypass valve during plant start
Enforcement action does not apply because the performance deficiency did not violate regulatory requirements. Because this finding does not involve a violation of regulatory requirements and has very low safety significance, it is characterized as a finding and is designated as FIN 05000458/2011004-02, Ineffective Corrective Actions on the Main Steam Equalizing Header Drain Bypass Valve Results in an Unplanned Down Power.
-up was a performance deficiency. Specifically, EN-LI-102, "Corrective Action Process," states that individuals are required to take immediate actions to resolve adverse conditions to minimize the consequence of the condition. Contrary to this, during refuelling outage 16, the outage control center and main control room personnel failed to adequately investigate the dual indications identified on the main steam equalizing header drain bypass valve. The finding was more than minor because it was associated with the equipment performance attribute of the initiating events cornerstone and affected the cornerstone objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions during shutdown as well as power operations.


The inspectors reviewed the finding using Inspection Manual Chapter 0609, Appendix A, "Significance Determination of Reactor Inspection Findings for At
===.4 Selected Issue Follow-up Inspection===
-Power Situations."
a.


Based on the Phase 1 screening of the finding, the inspectors determined that the finding was of very low safety significance (Green) because it was not a loss of coolant accident initiator, did not contribute to both the likelihood of an initiating event and the likelihood that mitigating equipment or functions would not be available, nor increase the likelihood of an external event (seismic, flooding
During a review of items entered in the licensees corrective action program, the inspectors recognized a corrective action item documenting a human performance error involving an operator performing maintenance on the emergency diesel generator without a work order. The inspectors discussed the event with licensee management, engineering, and operations to understand the human performance error and the scope of the corrective actions taken by the licensee. The inspectors determined that the error was a minor violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, for performing maintenance on the emergency diesel generator lube oil strainer without appropriate work instructions.
, or severe weather event)
. The apparent cause of the performance deficiency was that the control room and outage control center personnel presumed that the main control room dual indication for the valve was incorrect because previously valve operation successfully closed the valve
. Consequently, this finding has a crosscutting aspect in the area of human performance associated with the decision-making component because station personnel failed to use a systematic process to assess the condition of the bypass valve, and failed to verify the validity of the underlying assumptions that were used to justify operation with the valve having dual indication
[H.1(a)].


=====Enforcement.=====
Inspection Scope
Enforcement action does not apply because the performance deficiency did not violat e regulatory requirements.


Because this finding does not involve a violation of regulatory requirements and has very low safety significance, it is characterized as a finding and is designated as FIN 05000458/20110 0 4-0 2, "Ineffective Corrective Actions on the Main Steam Equalizing Header Drain Bypass Valve Results in an Unplanned Down Power."
These activities constitute completion of one in-depth problem identification and resolution sample as defined in Inspection Procedure 71152-05.


===.4 Selected Issue Follow===
b.


-up Inspection a. During a review of items entered in the licensee's corrective action program, the inspectors recognized a corrective action item documenting a human performance error involving an operator performing maintenance on the emergency diesel generator without a work order. The inspectors discussed the event with licensee management, engineering, and operations to understand the human performance error and the scope of the corrective actions taken by the licensee. The inspectors determined that the error was a minor violation of 10 CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," for performing maintenance on the emergency diesel generator lube oil strainer without appropriate work instructions.
No findings were identified.


Inspection Scope These activities constitute completion of one in-depth problem identification and resolution sample as defined in Inspection Procedure
Findings


==71152 - 05.==
===.5 Selected Issue Follow-up Inspection===
b. No findings were identified.
a.


Findings
During a review of items entered in the licensees corrective action program, the inspectors recognized a corrective action item documenting multiple human performance errors involving a misalignment of the reactor water cleanup system. The inspectors discussed the event with licensee management and operations to understand the human performance errors and the scope of the corrective actions taken by the licensee. The inspectors determined that the error was a minor violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, for failure to follow procedure.


===.5 Selected Issue Follow===
Inspection Scope


-up Inspection a. During a review of items entered in the licensee's corrective action program, the inspectors recognized a corrective action item documenting multiple human performance errors involving a misalignment of the reactor water cleanup system. The inspectors discussed the event with licensee management and operations to understand the human performance errors and the scope of the corrective actions taken by the licensee. The inspectors determined that the error was a minor violation of 10 CFR Part 50 , Appendix B, Criterion V, "Instructions, Procedures, and Drawings," for failure to follow procedure.
These activities constitute completion of one in-depth problem identification and resolution sample as defined in Inspection Procedure 71152-05.


Inspection Scope These activities constitute completion of one in-depth problem identification and resolution sample as defined in Inspection Procedure
b.


==71152 - 05.==
No findings were identified.
b. No findings were identified.


Findings  
Findings  
{{a|4OA6}}
{{a|4OA6}}
==4OA6 Meetings Exit Meeting==


Summary On September 16, 2011, the inspectors presented the results of the radiation safety inspections to Mr. E. Olson, Site Vice President, and other members of the licensee staff. The licensee acknowledged the issues presented. The inspectors asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.
==4OA6 Meetings==
===Exit Meeting Summary===
On September 16, 2011, the inspectors presented the results of the radiation safety inspections to Mr. E. Olson, Site Vice President, and other members of the licensee staff. The licensee acknowledged the issues presented. The inspectors asked the licensee whether any materials  
 
examined during the inspection should be considered proprietary. No proprietary information was identified.


On October 12, 2011, the inspectors presented the integrated inspection results to Mr. E. Olson, Site Vice President, and other members of the licensee staff. The licensee acknowledged the issues presented. The inspector asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.
On October 12, 2011, the inspectors presented the integrated inspection results to Mr. E. Olson, Site Vice President, and other members of the licensee staff. The licensee acknowledged the issues presented. The inspector asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.


{{a|4OA7}}
{{a|4OA7}}
==4OA7 Licensee-Identified Violations==
==4OA7 Licensee-Identified Violations==
The following violations of very low safety significance (Green) were identified by the licensee and are violations of NRC requirements which meet the criteria of Section 2.3.2 of the NRC Enforcement Policy for being dispositioned as noncited violations:
The following violations of very low safety significance (Green) were identified by the licensee and are violations of NRC requirements which meet the criteria of Section 2.3.2 of the NRC Enforcement Policy for being dispositioned as noncited violations:


===.1 Title 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," states, in part, that measures shall be established to assure that conditions adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and equipment, and nonconformances are promptly identified and corrected.===
===.1 Title 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, states, in part, that===
Contrary to these requirements, the licensee took incomplete measures to ensure the completion of slow turbine rolls to remediate the air voiding in the lube oil system of the reactor core isolation cooling turbine. On April 17, 2010, operations reported a low oil level in both sight glasses of the reactor core isolation cooling turbine.
measures shall be established to assure that conditions adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and equipment, and nonconformances are promptly identified and corrected. Contrary to these requirements, the licensee took incomplete measures to ensure the completion of slow turbine rolls to remediate the air voiding in the lube oil system of the reactor core isolation cooling turbine. On April 17, 2010, operations reported a low oil level in both sight glasses of the reactor core isolation cooling turbine. The investigation attributed the cause of the low oil level as a failure to perform a slow roll on the reactor core isolation cooling turbine following system maintenance. On February 10, 2011, during the plant start-up from refueling outage 17, station management canceled the work order to perform the slow roll of the reactor core isolation cooling turbine following lube oil system maintenance, resulting in air accumulating in the lube oil system. The finding was considered to be of very low safety significance (Green) because it was not a design or qualification deficiency; did not represent either a loss of system safety function, an actual loss of safety function of a single train, or an actual loss of safety function; and did not screen as potentially risk significant due to a seismic, flooding, or severe weather initiating event. The issue has been entered into the licensees corrective action program as Condition Report CR-RBS-2010-03854.


The investigation attributed the cause of the low oil level as a failure to perform a slow roll on the reactor core isolation cooling turbine following system maintenance.
===.2 Technical Specification 5.4.1 requires that written procedures shall be established,===
implemented, and maintained covering, in part, the applicable procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978. In RG 1.33, section 9 of Appendix A says, in part, that maintenance that can affect the performance of safety-related equipment should be performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances. Contrary to the above, between February 4, 2011, and February 7, 2011 the licensee performed maintenance that could affect the performance of safety-related equipment in accordance with documented instructions that were not appropriate to the circumstances, in that:
* Removing temporary filter media installed in safety-related unit coolers was maintenance that could affect the performance of safety-related equipment.
* Removal of filter media was performed in accordance with task 02 of work order 230363.
* Although task 02 of work order 230363 identified the unit coolers from which filter media were to be removed, task 02 of work order 230363 did not include details that described behind which unit cooler door the media were located. It also did not include criteria for determining that the media had been successfully removed.


On February 10, 2011, during the plant start
As a result, on March 3, 2011, a worker assigned to verify that filter media had been removed from safety-related unit coolers via task 02 of work order 230363 failed to locate the installed filter media and signed off on the work order to indicate that the media had been removed. This issue is addressed in the licensees corrective action program in Condition Report CR-RBS-2010-04331.
-up from refueling outage 17, station management canceled the work order to perform the slow roll of the reactor core isolation cooling turbine following lube oil system maintenance, resulting in air accumulating in the lube oil system. The finding was considered to be of very low safety significance (Green) because it was not a design or qualification deficiency; did not represent either a loss of system safety function, an actual loss of safety function of a single train, or an actual loss of safety function; and did not screen as potentially risk significant due to a seismic, flooding, or severe weather initiating event.


The issue has been entered into the licensee's corrective action program as Condition Report CR-RBS-2010-03854.
===.3 Technical Specification 5.4.1 requires that written procedures shall be established,===
implemented, and maintained covering, in part, the applicable procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978. In RG 1.33, section 9 of Appendix A says, in part, that maintenance that can affect the performance of safety-related equipment should be performed in accordance with written procedures appropriate to the circumstances. EN-WM-102, Work Implementation and Closeout, constituted documented instructions that were appropriate to the circumstances of performing maintenance that could affect the performance of safety-related equipment.


===.2 Technical Specification 5.4.1 requires that written procedures shall be established, implemented, and maintained covering, in part, the applicable procedures recommended===
Removing temporary filter media from various unit coolers as described in task 02 of work order 230363 was maintenance that could affect the performance of safety-related equipment. Contrary to the above, on February 7, 2011, before workers had completed task 02 of work order 230363, a Supervisor/Lead Worker set the status of that task to FINISHED within the work-control database without reviewing the associated task paperwork for signoffs/signatures. As a result, task 02 of work order 230363 was not completed, and temporary filter media remained in several unit coolers as the licensee started up the plant and returned it to full power. This issue is addressed in the licensees corrective action program in Condition Report CR-RBS-2010-04331.


in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.
===.4 Technical Specification 5.4.1 requires that written procedures shall be established,===
implemented, and maintained covering, in part, the applicable procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978. In RG 1.33, section 9 of Appendix A says, in part, that maintenance that can affect the performance of safety-related equipment should be performed in accordance with written procedures appropriate to the circumstances. Procedure EN-MA-101, Fundamentals of Maintenance, Rev. 9, in part, requires workers to place the equipment being worked on in a safe condition and contact their supervisor if any unexpected condition, event or results occur during the performance of the job. It also requires the worker to initiate a corresponding Condition Report. Contrary to the above, on March 3, 2011, after the licensee had discovered that not all signatures had been entered into task 02 of work order 230363 and a Mechanical Maintenance worker had been assigned to verify that the filter media installed under task 01 of work order 230363 had been removed, an unexpected condition occurred, in that although task 02 of work order 230363 indicated that some filter media were still installed, the worker found no filter media where he looked. When this occurred, that worker did not contact his supervisor and did not


In RG 1.33, section 9 of Appendix A says, in part, that maintenance that can affect the performance of safety
initiate a condition report. Instead, the worker signed task 02 of work order 230363 to indicate that the media had been removed. As a result, temporary filter media that should have been but were not removed via that task at the end of the refueling outage remained in several unit coolers as the plant operated at full power. This issue is addressed in the licensees corrective action program in Condition Report CR-RBS-2010-04331.
-related equipment should be performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances. Contrary to the above, between February 4, 2011, and February 7, 2011 the licensee performed maintenance that could affect the performance of safety
-related equipment in accordance with documented instructions that were not appropriate to the circumstances, in that:
Removing temporary filter media installed in safety
-related unit coolers was maintenance that could affect the performance of safety
-related equipment.


Removal of filter media was performed in accordance with task 02 of work order 230363. Although task 02 of work order 230363 identified the unit coolers from which filter media were to be removed, task 02 of work order 230363 did not include details that described behind which unit cooler door the media were located. It also did not include criteria for determining that the media had been successfully removed.
===.5 Title 10 CFR 50 Appendix B, Criterion XVI, Corrective Action, states, in part, that===
 
measures shall be established to assure that conditions adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and equipment, and nonconformances are promptly identified and corrected. Contrary to these requirements, plant personnel failed to properly evaluate and correct a damaged temperature control valve on the Division II emergency diesel generator jacket water system. During maintenance on the valve, the valve bonnet assembly fell approximately three feet from the top of the work table to the concrete floor causing a bend in the valve crank frame, which is a non-pressure retaining part. A condition report documented the damage, but station management failed to perform a formal assessment or a use as-is evaluation before installing the damaged pressure control valve bonnet assembly back into the valve body on the Division II emergency diesel generator. The finding is considered to be of very low safety significance (Green), because it was not a design or qualification deficiency; did not represent either a loss of system safety function, an actual loss of safety function of a single train, or an actual loss of safety function; and did not screen as potentially risk significant due to a seismic, flooding, or severe weather initiating event. The issue has been entered into the licensees corrective action program as condition report CR-RBS-2010-04785.
As a result, on March 3, 2011, a worker assigned to verify that filter media had been removed from safety
-related unit coolers via task 02 of work order 230363 failed to locate the installed filter media and signed off on the work order to indicate that the media had been removed. This issue is addressed in the licensee's corrective action program in Condition Report CR
-RBS-2010-04331.
 
===.3 Technical Specification 5.4.1 requires that written procedures shall be established, implemented, and maintained covering, in part, the applicable procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.===
In RG 1.33, section 9 of Appendix A says, in part, that maintenance that can affect the performance of safety
-related equipment should be performed in accordance with written procedures appropriate to the circumstances.
 
EN-WM-102, "Work Implementation and Closeout", constituted documented instructions that were appropriate to the circumstances of performing maintenance that could affect the performance of safety
-related equipment. Removing temporary filter media from various unit coolers as described in task 02 of work order 230363 was maintenance that could affect the performance of safety
-related equipment. Contrary to the above, on February 7, 2011, before workers had completed task 02 of work order 230363, a Supervisor/Lead Worker set the status of that task to "FINISHED" within the work
-control database without reviewing the associated task paperwork for signoffs/signatures. As a result, task 02 of work order 230363 was not completed, and temporary filter media remained in several unit coolers as the licensee started up the plant and returned it to full power. This issue is addressed in the licensee's corrective action program in Condition Report CR
-RBS-2010-04331.
 
===.4 Technical Specification 5.4.1 requires that written procedures shall be established, implemented, and maintained covering, in part, the applicable procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.===
In RG 1.33, section 9 of Appendix A says, in part, that maintenance that can affect the performance of safety
-related equipment should be performed in accordance with written procedures appropriate to the circumstances.
 
Procedure EN
-MA-101, "Fundamentals of Maintenance", Rev. 9, in part, requires workers to place the equipment being worked on in a safe condition and contact their supervisor if any unexpected condition, event or results occur during the performance of the job.
 
It also requires the worker to initiate a corresponding Condition Report. Contrary to the above, on March 3, 2011, after the licensee had discovered that not all signatures had been entered into task 02 of work order 230363 and a Mechanical Maintenance worker had been assigned to verify that the filter media installed under task 01 of work order 230363 had been removed, an unexpected condition occurred, in that although task 02 of work order 230363 indicated that some filter media were still installed, the worker found no filter media where he looked. When this occurred, that worker did not contact his supervisor and did not initiate a condition report. Instead, the worker signed task 02 of work order 230363 to indicate that the media had been removed.
 
As a result, temporary filter media that should have been but were not removed via that task at the end of the refueling outage remained in several unit coolers as the plant operated at full power.
 
This issue is addressed in the licensee's corrective action program in Condition Report CR
-RBS-2010-04331.
 
===.5 Title 10 CFR 50 Appendix B, Criterion XVI, Corrective Action, states, in part, that measures shall be established to assure that conditions adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and equipment, and nonconformances are promptly identified and corrected.===
 
Contrary to these requirements, plant personnel failed to properly evaluate and correct a damaged temperature control valve on the Division II emergency diesel generator jacket water system. During maintenance on the valve, the valve bonnet assembly fell approximately three feet from the top of the work table to the concrete floor causing a bend in the valve crank frame, which is a non
-pressure retaining part.
 
A condition report documented the damage, but station management failed to perform a formal assessment or a "use as
-is evaluation" before installing the damaged pressure control valve bonnet assembly back into the valve body on the Division II emergency diesel generator.
 
The finding is considered to be of very low safety significance (Green), because it was not a design or qualification deficiency; did not represent either a loss of system safety function, an actual loss of safety function of a single train, or an actual loss of safety function; and did not screen as potentially risk significant due to a seismic, flooding, or severe weather initiating event. The issue has been entered into the licensee's corrective action program as condition report CR-RBS-2010-04785.


=SUPPLEMENTAL INFORMATION=
=SUPPLEMENTAL INFORMATION=


==KEY POINTS OF CONTACT==
==KEY POINTS OF CONTACT==
===Licensee Personnel===
===Licensee Personnel===
: [[contact::D. Burnett]], Manager, Emergency Preparedness  
: [[contact::D. Burnett]], Manager, Emergency Preparedness  
: [[contact::G. Bush]], Manager, Material, Procurement, and Contracts  
: [[contact::G. Bush]], Manager, Material, Procurement, and Contracts  
: [[contact::M. Chase]], Manager, Training  
: [[contact::M. Chase]], Manager, Training  
: [[contact::W. Chatterton]], Sr. Lead Technical Specialist, Program & Components Engineering
: [[contact::W. Chatterton]], Sr. Lead Technical Specialist, Program & Components Engineering  
: [[contact::H. Choate]], Engineer, System Engineering
: [[contact::H. Choate]], Engineer, System Engineering  
: [[contact::J. Clark]], Manager, Licensing  
: [[contact::J. Clark]], Manager, Licensing  
: [[contact::L. Coats]], Senior Health Physicist/Chemistry Specialist
: [[contact::L. Coats]], Senior Health Physicist/Chemistry Specialist  
: [[contact::C. Colman]], Manager, Engineering Programs & Components  
: [[contact::C. Colman]], Manager, Engineering Programs & Components  
: [[contact::F. Corley]], Manager, Design Engineering  
: [[contact::F. Corley]], Manager, Design Engineering  
Line 694: Line 757:
: [[contact::M. Feltner]], Manager, Planning and Scheduling, Outages  
: [[contact::M. Feltner]], Manager, Planning and Scheduling, Outages  
: [[contact::C. Forpahl]], Manager, System Engineering  
: [[contact::C. Forpahl]], Manager, System Engineering  
: [[contact::A. Fredieu]], Manager, Outage
: [[contact::A. Fredieu]], Manager, Outage  
: [[contact::W. Fountain]], Senior Licensing Specialist  
: [[contact::W. Fountain]], Senior Licensing Specialist  
: [[contact::R. Gadbois]], General Manager, Plant Operations  
: [[contact::R. Gadbois]], General Manager, Plant Operations  
: [[contact::T. Gates]], Assistant Operations Manager  
: [[contact::T. Gates]], Assistant Operations Manager - Shift  
- Shift
: [[contact::H. Goodman]], Director, Engineering  
: [[contact::H. Goodman]], Director, Engineering  
: [[contact::D. Heath]], Supervisor, Radiation Protection
: [[contact::D. Heath]], Supervisor, Radiation Protection  
: [[contact::R. Heath]], Manager, Chemistry  
: [[contact::R. Heath]], Manager, Chemistry  
: [[contact::K. Huffstatler]], Senior Licensing Specialist  
: [[contact::K. Huffstatler]], Senior Licensing Specialist  
: [[contact::L. Kitchen]], Manager, Maintenance  
: [[contact::L. Kitchen]], Manager, Maintenance  
: [[contact::G. Krause]], Assistant Operations Manager  
: [[contact::G. Krause]], Assistant Operations Manager - Support  
- Support
: [[contact::E. Olson]], Site Vice President  
: [[contact::E. Olson]], Site Vice President  
: [[contact::R. Persons]], Superintendent, Training  
: [[contact::R. Persons]], Superintendent, Training  
: [[contact::G. Pierce]], Manager, Radiation Protection  
: [[contact::G. Pierce]], Manager, Radiation Protection  
: [[contact::J. Roberts]], Director, Nuclear Safety Assurance
: [[contact::J. Roberts]], Director, Nuclear Safety Assurance  
: [[contact::J. Schlesinger]], Senior Engineer, Design Engineering
: [[contact::J. Schlesinger]], Senior Engineer, Design Engineering  
: [[contact::T. Shenk]], Assistant Operations Manager  
: [[contact::T. Shenk]], Assistant Operations Manager - Training  
- Training
: [[contact::W. Spell]], Senior Health Physicist/Chemistry Specialist  
: [[contact::W. Spell]], Senior Health Physicist/Chemistry Specialist
: [[contact::M. Spustack]], Supervisor, Engineering  
: [[contact::M. Spustack]], Supervisor, Engineering  
: [[contact::J. Standridge]], Planner, Emergency
: [[contact::J. Standridge]], Planner, Emergency Preparedness  
Preparedness  
: [[contact::N. Tison]], Planner, Emergency Preparedness  
: [[contact::N. Tison]], Planner, Emergency Preparedness  
: [[contact::D. Vines]], Manager, Corrective Actions and Assessments  
: [[contact::D. Vines]], Manager, Corrective Actions and Assessments  
: [[contact::J. Vukovics]], Supervisor, Reactor Engineering  
: [[contact::J. Vukovics]], Supervisor, Reactor Engineering  
: [[contact::J. Wilson]], Supervisor, System Engineering
: [[contact::J. Wilson]], Supervisor, System Engineering  
: [[contact::L. Woods]], Manager, Quality Assurance
: [[contact::L. Woods]], Manager, Quality Assurance  
: [[contact::S. Zabaski]], Senior Health Physicist/Chemistry Specialist
: [[contact::S. Zabaski]], Senior Health Physicist/Chemistry Specialist  
 
Attachment


==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==
==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==
===Opened and Closed===
===Opened and Closed===
: 05000458/2011004
: 05000458/2011004-01 NCV Inadequate Standby Gas Treatment Electric Heater Power Output Calculation  
-0 1 NCV Inadequate Standby Gas Treatment Electric Heater Power Output Calculation
: 05000458/2011004-02 FIN Ineffective Corrective Actions on the Main Steam Equalizing Header Drain Bypass Valve Results in an Unplanned Down Power  
: 05000458/2011004
-0 2 FIN Ineffective Corrective Actions on the Main Steam Equalizing Header Drain Bypass Valve Results in an Unplanned Down Power


==LIST OF DOCUMENTS REVIEWED==
==LIST OF DOCUMENTS REVIEWED==
==Section 1R01: Adverse Weather Protection==
: PROCEDURES
: NUMBER TITLE REVISION/DATE
: ADM-0096 Risk Management Program and Implementation Risk Assessment
: 10
: ENS-DC-199 Off-Site Power Supply Design Requirements
: ENS-DC-201 Transmission Grid Monitoring Section 1R
: 04:
: Equipment Alignment
: CONDITION REPORTS
: CR-RBS-2011-03758
: CR-RBS-2011-03898
: CR-RBS-2011-04786
: CR-RBS-2011-05218
: CR-RBS-2011-05236
: CR-RBS-2011-05252
: CR-RBS-2011-05611
: CR-RBS-2011-06058
: CR-RBS-2011-06189
: CR-RBS-2011-06232
: DRAWINGS
: NUMBER TITLE REVISION
: PID-09-08A System 102
- Bearing Cooling Water
: PID-09-10A System 118
- Service Water
- Normal 33
: PID-09-10B System 118
- Service Water
- Normal 43
: PID-09-10D System 118
- Service Water
- Normal 34
: PID-09-10E System 256
- Service Water
- Standby 20 
: Attachment
: PID-09-10F System 118 - Service Water
- Normal 29
: PID-09-10H System 118
- Service Water
- Normal 26
: PID-27-06A System 209
- Reactor Core Isolation Cooling
: PID-27-15A System 257
- Standby Gas Treatment
: PID-27-20A System 208
- MSIV Positive Leakage Control
: PID-27-20C System 208
- LSV*C3A Compressor Skid
: PROCEDURES
: NUMBER TITLE REVISION
: SOP-0034 MSIV Sealing System (Positive Leakage Control) and Penetration Valve Leakage Control (SYS #208/255) 011
: SOP-0035 Reactor Core Isolation Cooling System (SYS #209)
: 038
: SOP-0042 Standby Service Water System (SYS #256)
: 033
: SOP-0043 Standby Gas Treatment System (SYS #257)
: 015
: Section 1R
: 05:
: Fire Protection
: CONDITION REPORTS
: CR-RBS-2011-04868
: CR-RBS-2011-04895
: CR-RBS-2011-05784
: CR-RBS-2011-05882
: CR-RBS-2011-06219
: PROCEDURES
: NUMBER TITLE REVISION
: AB-070-408 D-Tunnel Fire Area
: AB-7 1
: AB-070-503 RCIC Pump Room fire Area AB
-4/Z-1 and Z-2 4
: RW-106 Radwaste Building Elevation 106'
: Attachment
: RIVER BEND STATION UPDATED SAFETY ANALYSIS REPORT
: SECTION TITLE 9A.1 Introduction Section 1R
: 07:
: Heat Sink Performance
: CALCULATION
: NUMBER TITLE REVISION G13.18.2.1*061
: Auxiliary Building Design Basis Heat Loads and Unit Cooler Sizing Verification
: CONDITION REPORTS
: CR-RBS-2011-04331
: CR-RBS-2011-04924
: CR-RBS-2011-05616
: CR-RBS-2011-05867
: CR-RBS-2011-05878
: LO-WTRBS-2011-00047
: ENGINEERING REQUESTS
: NUMBER TITLE REVISION
: ER 99-0464 Insulation of Piping in the Auxiliary Building for Margin Recovery of Unit Coolers HVR
-UC3, 4, 6, 7, 9, & 10 0
: ER-99-0464, ER Change Notice Additional Insulation was Installed on RHS and CSH Piping Lines Outside the Final Scope ER 99
-0464 0
: ER 99-0690 Design Margin Recovery for Aux. Building Unit Coolers Using 95F Max. Service Water Temperature vs. 96F Used in Original HVAC Design 0
: PROCEDURE
: NUMBER TITLE REVISION R-STM-0403 Reactor Building HVAC System
: WORK ORDERS
: WO 00175720
: WO 00247094
: Attachment
: OTHER
: NUMBER TITLE REVISION/DATE
: Generic Letter
: GL 89-13 Service Water System Problems Affecting Safety
-Related Equipment July 18, 1989
===Vendor Document===
: No. NESE 908
: Auxiliary Building Unit Cooler Performance at 95 F Service Water Temperature
==Section 1R11: Licensed Operator Requalification Program==
: CONDITION REPORT
: CR-RBS-2011-06344
: SCENARIO
: NUMBER TITLE REVISION
: RSMS-OPS-813 Loss of NPS
-SWG1B/MSIV Isolation/Open SRV
==Section 1R12: Maintenance Effectiveness==
: CONDITION REPORTS
: CR-RBS-2009-04870
: CR-RBS-2009-05849
: CR-RBS-2010-01570
: CR-RBS-2010-05293
: CR-RBS-2011-01826
: CR-RBS-2011-02081
: CR-RBS-2011-03644
: CR-RBS-2011-03675
: CR-RBS-2011-05065
: MAINTENANCE RULE PROGRAM DOCUMENTS
: NUMBER TITLE REVISION Engineering Report #RBS-SE-11-00001 Maintenance Rule (a)(3) Periodic Assessment
: 2009-10 0 Engineering Report
#RBS-CS-05-00001 2005 Maintenance Rule Structures Periodic Assessment
: Attachment
: PROCEDURES
: NUMBER TITLE REVISION
: EDP-CS-15 River Bend Station Maintenance Rule Structural Monitoring Procedure
: 2
: EN-DC-150 Condition Monitoring of Maintenance Rule Structures
: EN-DC-167 Classification of Structures, Systems, and Components
: EN-DC-203 Maintenance Rule Program
: RIVER BEND STATION UPDATED SAFETY ANALYSIS REPORT
: SECTION TITLE 3.8 Design of Category I Structures
: WORK ORDERS
: WO 00091101
: WO 00110982
: WO 00117266
: WO 00148551
: WO 00149130
: WO 00182710
: WO 00182711
: WO 00194017
: WO 00200058
: WO 00214835
: WO 00238543
: WO 00238544 WO 00238930
: WO 00258978
: WO 00264289
==Section 1R13: Maintenance Risk Assessment and Emergent Work Controls==
: CONDITION REPORTS
: CR-RBS-2011-04792
: CR-RBS-2011-05987
: PROCEDURE
: NUMBER TITLE REVISION
: ADM-0096 Risk Management Program Implementation and On-Line Maintenance Risk Assessment
: 309
: STP-204-4509 LPCI Pump B Discharge Flow
- Low, Channel Functional Test
: STP-204-4510 LPCI Pump C Discharge Flow
- Low, Channel Functional Test
: Attachment
==Section 1R15: Operability Evaluations==
: CONDITION REPORTS
: CR-RBS-2009-03907
: CR-RBS-2010-00005
: CR-RBS-2010-04835
: CR-RBS-2011-04785
: CR-RBS-2011-04835
: CR-RBS-2011-04933
: CR-RBS-2011-05504
: CR-RBS-2011-05504
: CR-RBS-2011-05811
: CR-RBS-2011-05992
: CR-RBS-2011-05992
: CR-RBS-2011-06369
: CR-RBS-2011-06599
: LO-NOE-2005-00022
: DRAWINGS
: NUMBER TITLE REVISION
: EE-003KY Wiring Diagram
- Leakage Panels LSV
-PNL55A &
: LSV-PNL55B 11
: ESK-06LSV11, Sheet 2 Elementary Diagram
- 480V Control Circuit Pen Valves Leakage Control Air Compressor
: ESK-07LSV06, Sheet 1 Elementary Diagram
- 120VAC Control CKT Leakage Cont Air Cprsr 1LSV*C3B, 1LSV*PNL55B
: ESK-10IHA224, Sheet 1 Digital Isolator Circuits
- Isolator Circuits DIV I, DIV
: II 7
: KA-EP-119AA, Sheet 1 Sleeve Details Auxiliary Building
: ENGINEERING CHANGE
: S
: NUMBER TITLE REVISION
: EC-17980 Engineering Evaluation to Provide Alternate Repair Methodologies for Degraded Flexible Conduit Jackets 0
: EC-31479 Relocation of LSV
-LC46B to Originally Specified Location 0
: RIVER BEND STATION TECHNICAL SPECIFICATION
: NUMBER TITLE AMENDMENT/REVISION
: B3.3.5.2 RCIC System Instrumentation
: Attachment
: WORK ORDER
: WO 00288114
: OTHER
: NUMBER TITLE REVISION/DATE Engineering Report
: RBS-ME-08-00001 Summary of Activities Associated with the Resolution of GL 2008
-01 0 Promatec Final Report CTP
-1033 Differential Pressure Test LDSE
- 4" Depth Mechanical December 14, 1983
: Specification Number 229.180
: Floor and Wall Sleeve Seals
==Section 1R18: Plant Modifications==
: CONDITION REPORTS
: CR-RBS-1996-00390
: CR-RBS-2011-03037
: CR-RBS-2011-03041
: CR-RBS-2011-03255
: CR-RBS-2011-06366
: CR-RBS-2011-06368
: CR-RBS-2011-06371
: CR-RBS-2011-06383
: CR-WF3-2010-06369
: DRAWINGS
: NUMBER TITLE REVISION
: EE-003KY Wiring Diagram
- Leakage Panels LSV
-PNL55A &
: LSV-PNL55B 11
: ESK-06LSV11, Sheet 2 Elementary Diagram
- 480V Control Circuit Pen Valves Leakage Control Air Compressor
: ESK-07LSV06, Sheet 1 Elementary Diagram
- 120VAC Control CKT Leakage Cont Air Cprsr 1LSV*C3B, 1LSV*PNL55B
: ESK-10IHA224, Sheet 1 Digital Isolator Circuits
- Isolator Circuits DIV I, DIV
: II 7
: ENGINEERING CHANGES
: NUMBER TITLE REVISION E
: C-28898 G33-EB002A Leak Repair Quantity Adjustment from
: EC-28545 0 
: Attachment
: EC-31398
: LSV-AOV44B Outlet Restricting Orifice
: EC-31479 Relocation of LSV
-LC46B to Originally Specified Location 0
: EC-31481 Reevaluate Seismic Qualification of Tank
: LSV-TK6B with Accumulated Moisture
: EC-31483 Remove Level Control Function for SWP
-SOV220B 0
: WORK ORDERS
: WO 00
: 284943 WO 00285929
: WO 00288114
: WO 00 288456
==Section 1R19: Postmaintenance Testing==
: CALCULATION
: S
: NUMBER TITLE REVISION/DATE
: G13.18.2.1*060
: Control Building Charcoal Filter Heater and Fuel Building Ventilation & Standby Gas Treatment System Charcoal Filter Heater Required Heat Dissipation
: G13.18.13.2*088
: Temperature and Inventory Effects of Maximum Safeguards Operation on the Ultimate Heat Sink (Standby Cooling Tower)
: CONDITION REPORTS
: CR-RBS-1995-00383
: CR-RBS-2011-04785
: CR-RBS-2011-05611
: CR-RBS-2011-05811
: CR-RBS-2011-05950
: CR-RBS-2011-06189
: CR-RBS-2011-06366
: CR-RBS-2011-06368
: CR-RBS-2011-06371
: CR-RBS-2011-06383
: CR-RBS-2011-06903
: CR-RBS-2011-06928
: CR-RBS-2011-06936
: CR-RBS-2011-06941
: CR-WF3-2010-02278
: CR-WF3-2010-06369
: DRAWING
: NUMBER TITLE REVISION
: PID-27-20D System 208
- LSV*C3B Compressor Skid
: Attachment
: ENGINEERING CHANGE
: S
: NUMBER TITLE REVISION
: EC-30850
: GTS-FLT1B Operation with One Heater Element Out of Service
: EC-31398
: LSV-AOV44B Outlet Restricting Orifice
: EC-31481 Reevaluate Seismic Qualification of Tank
: LSV-TK6B with Accumulated Moisture
: EC-31483 Remove Level Control Function for SWP
-SOV220B 0
: EC-31488 Revise References to LSV Separator Tank Levels in TMOD EC
-31483 0
: PROCEDURES
: NUMBER TITLE REVISION
: EN-MA-105 Control of Measuring and Test Equipment (M&TE)
: STP-257-0202 Standby Gas Treatment System Filter Train B Monthly Operability Test
: 013
: STP-302-0102 Power Distribution System Operability Check
: 017
: WORK ORDERS
: WO 00281193
: WO 00284943
: WO 00285929
: WO 50347934
: WO 52350242
: OTHER
: NUMBER TITLE DATE --- Main Control Room Log
- Days/Nights September 3, 2011
: Asset Number
: COM-128A Certificate of Calibration for Fluke Corporation 353
- True-rms AC/DC Clamp Meter July 6, 2011
: R-STM-206, Figure 4 Penetration Valve Leakage Control System
: N/A 
: Attachment
==Section 1R22: Surveillance Testing==
: CALCULATION
: NUMBER TITLE REVISION
: NEAD-SR-10/025 RBS SFP Racklife Update for Cycle 17 Operation
: CONDITION REPORTS
: CR-RBS-2007-05336
: CR-RBS-2011-05735
: CR-RBS-2011-06932
: PROCEDURES
: NUMBER TITLE REVISION
: REP-0007 Spent Fuel Pool Coupon Surveillance Program
: STP-204-4503 LPCI Pump A Discharge Flow
- Low, Channel Functional Test (1E12
-N652A) 5A
: STP-204-4509 LPCI Pump B Discharge Flow
- Low, Channel Functional Test (1E12
-N652B) 3
: RIVER BEND STATION UPDATED SAFETY ANALYSIS REPORT
: SECTION TITLE 9.1.2.4.2 Fuel Building Fuel Storage
: WORK ORDER
: WO 00113627
: OTHER
: NUMBER TITLE REVISION/DATE
--- RBS ECCS Test July 25, 2011
: Engineering Report
: ECH-NE-10-00089 BADGER Test Campaign at River Bend
: FPL LER 05000250/2010
-001-02 Spent Fuel Storage Design Feature Assumptions are Exceeded Supplement June 7, 2011
: Attachment
: NRC IN 2009
-26 Degradation of Neutron
-Absorbing Materials in the Spent Fuel Pool October 28, 2009
==Section 1EP6: Drill Evaluation==
: CONDITION REPORT
: CR-RBS-2011-05484
: PROCEDURES
: NUMBER TITLE REVISION
: EIP-2-006 Notifications
: RLEC-EP-115 EP Communications Standard
: SCENARIOS
: NUMBER TITLE REVISION
: RDRL-EP-1001 Site Drill Scenario
- Tornado, LOOP, SAE
- No
: GE 01
: RDRL-EP-1103 Unannounced Off
-Hours Staff Augmentation Drill
: RSMS-OPS-447 Fire in the Control Building Requiring Plant Shutdown 3
: Section 2RS06:
: Radioactive Gaseous and Liquid Effluent Treatment
: PROCEDURES
: NUMBER TITLE REVISION
: COP-0046 Sampling Gaseous Effluents Via The Wide Range Gas Monitors
: COP-0050 Grab Sampling Gaseous Waste Streams
: CSP-0110 Radioactive Liquid Effluent Batch Discharge
: EN-CY-111 Radiological Ground Water Monitoring
: RHP-0032 Dose Rate Calculations From Gaseous Effluents
: RSP-0008 Offsite Dose Calculation Manual
: Attachment
: AUDITS, SELF
-ASSESSMENTS, AND SURVEILLANCES
: NUMBER TITLE DATE S-CRB-24910 Combined Chemistry, Effluents, and Environmental Monitoring Programs September 10, 2009
: CONDITION REPORTS
: CR-RBS-2011-04124
: CR-RBS-2009-00653
: CR-RBS-2009-00746
: CR-RBS-2009-01083
: CR-RBS-2009-01085
: 10
: CFR 50.75 g CONDITION REPORTS
: CR-RBS-2010-02800
: CR-RBS-2010-03594
: LIQUID RELEASE PERMITS
: 2011006
: 2011054
: GASEOUS RELEASE
: NUMBER
: TITLE DATE
: RHP-0032 Data Package August 30, 2011
-
: September 6, 2011
: IN-PLACE FILTER TESTING RECORDS
: WORK ORDER SYSTEM TEST DATE
: 52271597 Division I Fuel Building Ventilation Laboratory Carbon Filter Analysis/STP
-406-8602 March 22, 2011
: 247398 Division l Standby Gas Treatment Laboratory Carbon Filter Analysis/STP
-257-8601 November 3, 2010
: 247005 Division II Fuel Building In-service Testing of HEPA and charcoal/
: STP-406-3602 March 30, 2011
: 233629 Division l Main Control Room Fresh Air Laboratory Carbon Filter Analysis/STP
-402-3601 April 6, 2010
: 52215840 Division II Fuel Building Ventilation Laboratory Carbon Filter Analysis/STP
-406-8603 March 5, 2010
: 210212 Division ll Standby Gas Treatment Laboratory Carbon Filter Analysis/STP
-257-8602 March 5, 2010
: Attachment
: 2196577 Division ll Control Room Fresh Air
: In-service Testing of HEPA and charcoal/
: STP-402-3602 March 15, 2010
: 00169452 Division l Control Room Fresh Air In-service Testing of HEPA and charcoal/
: STP-402-3601 April 6, 2010
: 276282 Division l Fuel Building In-service Testing of HEPA and charcoal/
: STP-406-3601 December 1, 2010
: EFFLUENT STACK AND VENT FLOW RATES
: WORK ORDER NUMBER TITLE DATE
: 52204969 Main Plant Exhaust Duct Monitoring System Flow March 9, 2010
: MISCELLANEOUS DOCUMENTS
: NUMBER TITLE DATE
: 2009 Annual Radioactive Effluent Release Report
: 2010 Annual Radioactive Effluent Release Report Section 2RS07:
: Radiological Environmental Monitoring Program
: PROCEDURES
: NUMBER TITLE REVISION
: EN-CY-111 Radiological Ground Water Monitoring
: EN-EV-100 Environmental Expectations
: EN-CY-109 Sampling and Analysis of Groundwater Monitoring Wells
: EN-RP-113 Response to Contaminated Spills/Leaks
: ESP-8-012 Routine Performance Checks of Meteorological Monitoring Equipment 15
: ESP-8-021 Sampling of Water for Radiological Environmental Monitoring
: ESP-8-023 Sampling of Airborne Radioiodine and Particulates for Radiological Environmental Monitoring
: Attachment
: ESP-8-027 Sampling of Botanical Specimens for Radiological Environmental Monitoring Program
: ESP-8-031 Analysis of Tritium Content in Water
: ESP-8-042 Radioactive Standard Preparation for Environmental Program 6
: ESP-8-052 Interlaboratory Comparison Program for Radiological Environmental Monitoring
: RSP-0008 Offsite Dose Calculation Manual
: AUDITS, SELF
-ASSESSMENTS, AND SURVEILLANCES
: NUMBER TITLE DATE S-CRB-24910 Combined Chemistry, Effluents, and Environmental Monitoring Programs September 10, 2009
: E 138/10 AREVA NP Environmental Laboratory
- Annual Quality Assurance Report for Environmental Analyses October 14, 2010
: CONDITION REPORTS
: HQN-2009-00113
: HQN-2010-00731
: HQN-2010-01279
: HQNLO-2008-00048
: RBS-2009-000780
: RBS-2009-01526
: RBS-2009-02702
: RBS-2009-05768
: RBS-2009-06507
: RBS-2010-01481
: RBS-2010-01547
: RBS-2010-02016
: RBS-2010-06587
: RBS-2011-00048
: RBS-2011-03262
: RBS-2011-03331
: RBS-2011-03681
: RBS-2011-04125
: RBS-2011-05250
: RBS-2011-05352
: WORK ORDERS
- CALIBRATIONS, MAINTENANCE, SURVEILLANCES, ETC.
: WO-RBS-51548-217 to 226
: WO-RBS-51650-362 to 365
: WO-RBS-51651-358 to 362
: WO-RBS-51652709
: WO-RBS-51696-113 to 122
: WO-RBS-52037-263 to 272
: WO-RBS-205532
: WO-RBS-52367205
: WO-RBS-52367206
: MISCELLANEOUS DOCUMENTS
: NUMBER TITLE REVISION
: Quality Assurance Program Manual Annual Radiological Environmental Operating Report for 2009
: Annual Radiological Environmental Operating Report for 2010
: Section 2RS08:
: Radioactive Solid Waste Processing and Radioactive Material handling, Storage, and Transportation
: PROCEDURES
: NUMBER TITLE REVISION
: EN-RW-102 Radioactive Shipping Procedure
: EN-RW-103 Radioactive Waste Tracking Procedure
: Attachment
: PROCEDURES
: NUMBER TITLE REVISION
: EN-RW-104 Scaling Factors
: EN-RW-105 Process Control Program
: EN-RP-121-01 Receipt of Radioactive Material
: RWS-0304 Radioactive Waste Handling and Control
: RWS-0336 Set-up and Operation of the RDS
-1000 Dewatering Unit
: AUDITS, SELF
-ASSESSMENTS, AND SURVEILLANCES
: NUMBER TITLE DATE
: QA 14/15-2009-RBS-1 Quality Assurance Audit Report November 2, 2009
-December 10, 2009
: QS-2010-RBS-009- S-CRB-24957 River Bend Quality Assurance Surveillance Report July 6,2010
-July 8, 2010
: QS-2010-RBS-007-SCRB 24955
: River Bend Quality Assurance Surveillance Report June 9, 2010
-June 11,2010
: CONDITION REPORTS
: 2009-00611 2009-01024 2009-01243 2009-01244 2009-02607 2010-01040 2010-01197 2010-02193 2010-02194 2010-02196 2010-04486 2010-06833 2011-00936 2011-03294 2011-03873 2011-04022 2011-05301 2011-05833 2011-06784 2011-06802 2011-06823
: RADIOACTIVE MATERIAL SHIPMENTS
: NUMBER TITLE DATE
: RBS-2009-107 Dive Sealand/Tungsten Shielding December 15, 2009
: RBS-2010-034 Mixed Bed Ion Exchange Media
- RWCU Powdex Resin June 24, 2010
: RBS-2011-006 8 Safety Relief Valves January 23, 2011
: RBS-2011-048 Mixed Bed Ion Exchange Media April 7, 2011
: RBS-2011-060 Upper Pool Sample April 25, 2011
: RBS-2011-061 RP Instruments April 21, 2011
==Section 4OA1: Performance Indicator Verification==
: OTHER
: NUMBER TITLE DATE
: RBG-47020 Electronic Submittal of First Quarter 2010 Performance Indicator Information April 21, 2010
: Attachment
: RBG-47053 Electronic Submittal of Second Quarter 2010 Performance Indicator Information July 21, 2010
: RBG-47106 Electronic Submittal of Fourth Quarter 2010
: Performance Indicator Information January 21, 2011
: RBG-47139 Electronic Submittal of First Quarter
: 2011 Performance Indicator Information April 21, 2011
: RBG-47164 Revision 22 to the Updated Safety Analysis Report August 5, 2011
: RBG-47165 Proposed Emergency Action Levels Using
: NEI 99-01 Revision 5 Scheme August 1, 2011
==Section 4OA2: Identification and Resolution of Problems==
: CONDITION REPORTS
: CR-RBS-2010-01600
: CR-RBS-2011-04485
: CR-RBS-2011-04592
: CR-RBS-2011-04747
: CR-RBS-2011-04954 CR-RBS-2011-05733


==Section 4OA7: Licensee-Identified Violations==
: CONDITION REPORTS
: CR-RBS-2011-04331
: CR-RBS-1999-00317
: CR-RBS-2011-00455
: CR-RBS-2011-3296
: CR-RBS-1999-0 0137
: PROCEDURES
: NUMBER TITLE REVISION
: EN-DC-335 PM Basis Template
: EN-DC-153 Preventative Maintenance Component Classification
: EN-AD-101 Procedure Process
: EN-LI-100 Process Applicability Determination
: EN-MA-101 Fundamentals of Maintenance
: EN-OP-119 Protected Equipment Postings
: EN-WM-100 Work Request (WR) Generation, Screening and Classification
: EN-WM-102 Work Implementation and Closeout
: EN-WM-105 Planning 9
: OTHER DOCUMENTS
: Work Order
: 293648 Work Order
: 230363
: ER 00-0099 Use of Exempt Items as Permanent Plant Equipment
: 0
}}
}}

Latest revision as of 22:20, 12 January 2025

IR 05000458-11-004; on 07/01/2011 – 09/30/2011; River Bend Station; Integrated Resident and Regional Report; Postmaintenance Testing
ML113140169
Person / Time
Site: River Bend Entergy icon.png
Issue date: 11/09/2011
From: Vincent Gaddy
NRC/RGN-IV/DRP/RPB-C
To: Olson E
Entergy Operations
References
IR-11-004
Download: ML113140169 (49)


Text

November 9, 2011

Eric Site Vice President Entergy Operations, Inc.

River Bend Station 5485 US Highway 61 St. Francisville, LA 70775

Subject: RIVER BEND STATION - NRC INTEGRATED INSPECTION REPORT NUMBER 05000458/2011004

Dear Mr. Olson:

On September 30, 2011, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your River Bend Station. The enclosed integrated inspection report documents the inspection findings, which were discussed on October 12, 2011, with you and other members of your staff.

The inspections examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

Based on the results of this inspection, the NRC has identified two issues that were evaluated under the risk significance determination process as having very low safety significance (Green). The NRC has determined that a violation was associated with one of these issues.

However, because of the very low safety significance and because it was entered into your corrective action program, the NRC is treating this finding as a noncited violation, consistent with Section 2.3.2 of the NRC Enforcement Policy. Additionally, five licensee-identified violations, which were determined to be of very low safety significance, are listed in this report.

If you contest the violations or the significance of the noncited violation, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, D.C.

20555-0001, with copies to the Regional Administrator, U.S. Nuclear Regulatory Commission, Region IV, 612 E. Lamar Blvd, Suite 400, Arlington, Texas, 76011-4125; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, D.C. 20555-0001; and the NRC Resident Inspector at the River Bend Station facility. In addition, if you disagree with the crosscutting aspect assigned to any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region IV, and the NRC Resident Inspector at River Bend Station.

UNITED STATES NUCLEAR REGULATORY COMMISSION

REGION IV

612 EAST LAMAR BLVD, SUITE 400 ARLINGTON, TEXAS 76011-4125

Entergy Operations, Inc.

- 2 -

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response, if you choose to provide one for cases where a response is not required, will be made available electronically for public inspection in the NRC Public Document Room or from the NRC's document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html. To the extent possible, your response should not include any personal privacy or proprietary information so that it can be made available to the public without redaction.

Sincerely, RC Hagar for V Gaddy Vincent G. Gaddy, Chief Project Branch C Division of Reactor Projects

Docket: 50-458 License: NPF-47

Enclosure:

NRC Inspection Report 05000458/2011004 w/Attachment: Supplemental Information

REGION IV==

Docket:

05000458 License:

NPF-47 Report:

05000458/2011004 Licensee:

Entergy Operations, Inc.

Facility:

River Bend Station Location:

5485 U.S. Highway 61 St. Francisville, LA Dates:

July 1 through September 30, 2011 Inspectors:

G. Larkin, Senior Resident Inspector, Project Branch C A. Barrett, Resident Inspector, Project Branch C R. Hagar, Senior Project Engineer, Project Branch C L. Ricketson, Senior Health Physicist, Plant Support Branch 2 B. Baca, Health Physicist, Technical Support Branch C. Alldredge, Health Physicist, Plant Support Branch 2 Approved By:

Vincent G. Gaddy, Chief, Project Branch C Division of Reactor Projects

- 2 -

Enclosure

SUMMARY OF FINDINGS

IR 05000458/2011004; 07/01/2011 - 09/30/2011; River Bend Station; Integrated Resident and

Regional Report; Postmaintenance Testing

The report covered a 3-month period of inspection by resident inspectors and an announced baseline inspection by region-based inspectors. One Green noncited violations and one Green finding of significance were identified. The significance of most findings is indicated by their color (Green, White, Yellow, or Red) using Inspection Manual Chapter 0609, Significance Determination Process. The crosscutting aspect is determined using Inspection Manual Chapter 0310, Components Within the Cross Cutting Areas. Findings for which the significance determination process does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process,

Revision 4, dated December 2006.

NRC-Identified Findings and Self-Revealing Findings

Cornerstone: Initiating Events

Green.

The inspectors identified a self-revealing finding involving inadequate corrective actions in response to a failure in the main steam equalizing header drain bypass valve, resulting in a steam leak and an unplanned plant down power. Specifically, plant personnel failed to properly address the dual indication on the bypass valve and fluid flow through the valve caused water to flash to steam accelerating pipe wall erosion and piping failure. The licensees immediate corrective actions were to identify, secure, and temporarily repair the steam leak. The licensee entered this issue into the licensees corrective action program as Condition Report CR-RBS-2011-04592.

The finding was more than minor because it was associated with the equipment performance attribute of the initiating events cornerstone and affected the cornerstone objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. The inspectors reviewed the finding using Inspection Manual Chapter 0609, Appendix A, Significance Determination of Reactor Inspection Findings for At-Power Situations. Based on the Phase 1 screening of the finding, the inspectors determined that the finding was of very low safety significance (Green) because it was not a loss of coolant accident initiator, did not contribute to both the likelihood of an initiating event and the likelihood that mitigating equipment or functions would not be available, nor increase the likelihood of an external event (seismic, flooding, or severe weather event). The apparent cause of the performance deficiency was that the control room and outage control center personnel presumed that the main control room dual indication for the valve was incorrect because previously valve operation successfully closed the valve. Consequently, this finding has a crosscutting aspect in the area of human performance associated with the decision-making component because station personnel did not use a systematic process to assess the condition of the bypass valve, and failed to verify the validity of the underlying assumptions that were used to justify operation with the valve having dual indications H.1(a)(Section 4OA2).

Cornerstone: Barrier Integrity

Green.

The inspectors identified a noncited violation of 10 CFR Part 50,

Appendix B, Criterion III Design Control, for an inadequate calculation methodology used in determining standby gas treatment system operability. The inspectors found that the calculation neither considered instrument uncertainty nor applied a proper voltage drop from the breaker to the standby gas treatment system filter train heater. The licensee entered this issue into the licensees corrective action program as Condition Report CR-RBS-2011-07332.

The finding was more than minor because it was associated with the design control attribute of the Barrier Integrity Cornerstone to maintain radiological barrier functionality of standby gas treatment trains, and affected the cornerstone objective to provide reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents or events.

Specifically, operating the standby gas system filter train heaters without sufficient output power is detrimental to the charcoal filters ability to retain radioactive iodine. This could result in a greater amount of radiation release to the environment in the event of an accident. In accordance with Inspection manual Chapter 0609, Appendix A, Significance Determination of Reactor Inspection Findings for At-Power Situations, the Phase 1 significance determination process screening determined the finding to be only of very low safety significance (Green) because the finding only represented a degradation of the radiological barrier function provided for the standby gas treatment system.

The apparent cause of this finding was the decision to develop an engineering evaluation that did not include instrument uncertainly and did not validate the correct voltage drop between the filter train heater feeder breaker and the heater elements. The finding has a crosscutting aspect in the area of human performance associated with the decision-making component because station personnel failed to use conservative assumptions when developing the modified output power methodology for operation of the standby gas treatment system filter heaters with only 8 of 9 heater elements installed H.1(b)(1R19 b.2).

Licensee-Identified Violations

Five violations of very low safety significance, which were identified by the licensee, have been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensees corrective action program. These violations and corrective action tracking numbers are listed in Section 4OA7.

REPORT DETAILS

Summary of Plant Status

River Bend Station began the inspection period at 100 percent rated thermal power. On July 8, 2011, the plant reduced reactor power to 66 percent to perform control rod insertion tests, perform turbine bypass valve testing, and complete a control rod sequence exchange.

The plant returned to full power on July 10, 2011. On September 23, 2011, the plant reduced reactor power to 61 percent to complete a control rod sequence exchange. The plant returned to full power on September 27, 2011, and remained at 100 percent reactor power for the remainder of the inspection period.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and Emergency Preparedness

1R01 Adverse Weather Protection

Summer Readiness for Offsite and Alternate-ac Power a.

The inspectors performed a review of preparations for summer weather for selected systems, including conditions that could lead to loss-of-offsite power and conditions that could result from high temperatures. The inspectors reviewed the procedures affecting these areas and the communications protocols between the transmission system operator and the plant to verify that the appropriate information was being exchanged when issues arose that could affect the offsite power system. Examples of aspects considered in the inspectors review included:

Inspection Scope

  • The coordination between the transmission system operator and the plants operations personnel during off-normal or emergency events
  • The explanations for the events
  • The estimates of when the offsite power system would be returned to a normal state
  • The notifications from the transmission system operator to the plant when the offsite power system was returned to normal

During the inspection, the inspectors focused on plant-specific design features and the procedures used by plant personnel to mitigate or respond to adverse weather conditions. Additionally, the inspectors reviewed the Updated Safety Analysis Report and performance requirements for systems selected for inspection, and verified that operator actions were appropriate as specified by plant-specific procedures. Specific

documents reviewed during this inspection are listed in the attachment. The inspectors also reviewed corrective action program items to verify that the licensee was identifying adverse weather issues at an appropriate threshold and entering them into their corrective action program in accordance with station corrective action procedures. The inspectors reviews focused specifically on the following plant systems:

These activities constitute completion of one readiness for summer weather effect on offsite and alternate-ac power sample as defined in Inspection Procedure 71111.01-05.

b.

No findings were identified.

Findings

1R04 Equipment Alignments

Partial Walkdown a.

The inspectors performed partial system walkdowns of the following risk-significant systems:

Inspection Scope

  • Standby gas treatment B during Division 1 surveillance
  • Division 1 main steam positive leakage control system while Division 2 was out of service for unplanned maintenance and troubleshooting

The inspectors selected these systems based on their risk significance relative to the reactor safety cornerstones at the time they were inspected. The inspectors attempted to identify any discrepancies that could affect the function of the system, and, therefore, potentially increase risk. The inspectors reviewed applicable operating procedures, system diagrams, Updated Safety Analysis Report, technical specification requirements, administrative technical specifications, outstanding work orders, condition reports, and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have rendered the systems incapable of performing their intended functions. The inspectors also inspected accessible portions of the systems to verify system components and support equipment were aligned correctly and operable. The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no obvious deficiencies. The

inspectors also verified that the licensee had properly identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the corrective action program with the appropriate significance characterization. Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of four partial system walkdown samples as defined in Inspection Procedure 71111.04-05.

b.

No findings were identified.

Findings

1R05 Fire Protection

.1 Quarterly Fire Inspection Tours

a.

The inspectors conducted fire protection walkdowns that were focused on availability, accessibility, and the condition of firefighting equipment in the following risk-significant plant areas:

Inspection Scope

  • July 19, 2011, D-Tunnel, fire area AB-7
  • July 29, 2011, radwaste building, 106-foot elevation, fire area RW-106
  • August 14, 2011, auxiliary building, 141-foot elevation and 98-foot elevation
  • August 16, 2011, normal switchgear building, 98-foot elevation and 123-foot elevation

The inspectors reviewed areas to assess if licensee personnel had implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant; effectively maintained fire detection and suppression capability; maintained passive fire protection features in good material condition; and had implemented adequate compensatory measures for out of service, degraded or inoperable fire protection equipment, systems, or features, in accordance with the licensees fire plan.

The inspectors selected fire areas based on their overall contribution to internal fire risk as documented in the plants Individual Plant Examination of External Events with later additional insights, their potential to affect equipment that could initiate or mitigate a plant transient, or their impact on the plants ability to respond to a security event. Using the documents listed in the attachment, the inspectors verified that fire hoses and extinguishers were in their designated locations and available for immediate use; that fire detectors and sprinklers were unobstructed; that transient material loading was

within the analyzed limits; and fire doors, dampers, and penetration seals appeared to be in satisfactory condition. The inspectors also verified that minor issues identified during the inspection were entered into the licensees corrective action program.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of five quarterly fire-protection inspection samples as defined in Inspection Procedure 71111.05-05.

b.

No findings were identified.

Findings

1R07 Heat Sink Performance

a.

The inspectors reviewed licensee programs, verified performance against industry standards, and reviewed critical operating parameters and maintenance records for the containment and auxiliary building unit coolers (both divisions). The inspectors verified that performance tests were satisfactorily conducted for heat exchangers/heat sinks and reviewed for problems or errors; the licensee utilized the periodic maintenance method outlined in EPRI Report NP 7552, Heat Exchanger Performance Monitoring Guidelines; the licensee properly utilized biofouling controls; the licensees heat exchanger inspections adequately assessed the state of cleanliness of their tubes; and the heat exchanger was correctly categorized under 10 CFR 50.65, Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants. Specific documents reviewed during this inspection are listed in the attachment.

Inspection Scope

These activities constitute completion of one heat sink inspection sample as defined in Inspection Procedure 71111.07-05.

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification Program

a.

On August 31, 2011, the inspectors observed a crew of licensed operators in the plants simulator to verify that operator performance was adequate, evaluators were identifying and documenting crew performance problems, and training was being conducted in accordance with licensee procedures. The inspectors evaluated the following areas:

Inspection Scope

  • Licensed operator performance
  • Crews clarity and formality of communications
  • Crews ability to take timely actions in the conservative direction
  • Crews prioritization, interpretation, and verification of annunciator alarms
  • Crews correct use and implementation of abnormal and emergency procedures
  • Control board manipulations
  • Oversight and direction from supervisors
  • Crews ability to identify and implement appropriate technical specification actions and emergency plan actions and notifications

The inspectors compared the crews performance in these areas to pre-established operator action expectations and successful critical task completion requirements.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one quarterly licensed-operator requalification program sample as defined in Inspection Procedure 71111.11.

b.

No findings were identified.

Findings

1R12 Maintenance Effectiveness

a.

The inspectors evaluated degraded performance issues involving the following risk significant systems:

Inspection Scope

  • Safety-related structures and the structural monitoring program

In addition, the inspectors reviewed the biennial Maintenance Rule (a)(3) report per the inspection guidance document.

The inspectors reviewed events such as where ineffective equipment maintenance has resulted in valid or invalid automatic actuations of engineered safeguards systems and independently verified the licensee's actions to address system performance or condition problems in terms of the following:

  • Implementing appropriate work practices
  • Identifying and addressing common cause failures
  • Characterizing system reliability issues for performance
  • Charging unavailability for performance
  • Trending key parameters for condition monitoring
  • Verifying appropriate performance criteria for structures, systems, and components classified as having an adequate demonstration of performance through preventive maintenance, as described in 10 CFR 50.65(a)(2), or as requiring the establishment of appropriate and adequate goals and corrective actions for systems classified as not having adequate performance, as described in 10 CFR 50.65(a)(1)

The inspectors assessed performance issues with respect to the reliability, availability, and condition monitoring of the system. In addition, the inspectors verified maintenance effectiveness issues were entered into the corrective action program with the appropriate significance characterization. Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of three quarterly maintenance effectiveness samples as defined in Inspection Procedure 71111.12-05.

b.

No findings were identified.

Findings

1R13 Maintenance Risk Assessments and Emergent Work Control

a.

The inspectors reviewed licensee personnel's evaluation and management of plant risk for the maintenance and emergent work activities affecting risk-significant and safety-related equipment listed below to verify that the appropriate risk assessments were performed prior to removing equipment for work:

Inspection Scope

  • Control rod drive pump failed postmaintenance testing, July 1, 2011
  • Emergent work in Fancy Point switchyard, August 8, 2011
  • Planned maintenance on the control room fresh air system, August 29, 2011
  • Planned maintenance on a service water cooling fan and heat exchanger, September 12, 2011
  • Elevated risk during RHR maintenance and switchyard work, September 13, 2011

The inspectors selected these activities based on potential risk significance relative to the reactor safety cornerstones. As applicable for each activity, the inspectors verified that licensee personnel performed risk assessments as required by 10 CFR 50.65(a)(4)and that the assessments were accurate and complete. When licensee personnel performed emergent work, the inspectors verified that the licensee personnel promptly assessed and managed plant risk. The inspectors reviewed the scope of maintenance work, discussed the results of the assessment with the licensee's probabilistic risk analyst or shift technical advisor, and verified plant conditions were consistent with the risk assessment. The inspectors also reviewed the technical specification requirements and inspected portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met. Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of five maintenance risk assessments and emergent work control inspection samples as defined in Inspection Procedure 71111.13-05.

b.

No findings were identified.

Findings

1R15 Operability Evaluations

a.

The inspectors reviewed the following issues:

Inspection Scope

  • CR-RBS-2011-05597, diesel generator thermostatic valve problem not identified promptly, reviewed on July 21, 2011
  • CR-RBS-2011-06063, E12-F048B flexible electrical conduit jacket degraded, reviewed on August 22, 2011

The inspectors selected these potential operability issues based on the risk significance of the associated components and systems. The inspectors evaluated the technical adequacy of the evaluations to ensure that technical specification operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the technical specifications and Updated Safety Analysis Report to the licensee personnels evaluations to determine whether the components or systems were operable. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. The inspectors determined, where appropriate, compliance with bounding limitations associated with the evaluations.

Additionally, the inspectors also reviewed a sampling of corrective action documents to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations. Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of six operability evaluation inspection samples as defined in Inspection Procedure 71111.15-04

b.

No findings were identified.

Findings

1R18 Plant Modifications

a.

Temporary Modifications To verify that the safety functions of important safety systems were not degraded, the inspectors reviewed the following temporary modifications:

Inspection Scope

  • Engineering Change EC-31398, LSV-AOV44B Outlet Restricting Orifice, Revision 0; Engineering Change EC-31483, Remove Level Control Function for SWP-SOV220B, Revision 0; and Engineering Change EC-31488, Revise References to LSV Separator Tank Levels in TMOD EC-31483, Revision 0
  • Engineering Change EC-30850, GTS-FLT1B Operation with One Heater Element Out of Service, Revision 0

The inspectors reviewed the temporary modifications and the associated safety-evaluation screening against the system design bases documentation, including the Updated Safety Analysis Report and the technical specifications, and verified that the modification did not adversely affect the system operability/availability. The inspectors also verified that the installation and restoration were consistent with the modification documents and that configuration control was adequate. Additionally, the inspectors verified that the temporary modification was identified on control room drawings, appropriate tags were placed on the affected equipment, and licensee personnel

evaluated the combined effects on mitigating systems and the integrity of radiological barriers.

These activities constitute completion of two samples for temporary plant modifications as defined in Inspection Procedure 71111.18-05.

b.

No findings were identified.

Findings

1R19 Postmaintenance Testing

a.

The inspectors reviewed the following postmaintenance activities to verify that procedures and test activities were adequate to ensure system operability and functional capability:

Inspection Scope

  • WO 00281193, EGT-TCV20B - Valve is Acting Irregularly (CR-11-4186),reviewed on July 5, 2011
  • WO 00284943, GTS-FLT1B During Performance of STP-257-0202 Discovered Low, reviewed on August 18, 2011
  • WO 00285929, LSV-C3B Water Leaking from LSV-STR10BB While in Service, reviewed on August 21, 2011
  • WO 00275198, Replace Relays ENB-INV01B1, reviewed on September 21, 2011
  • WO 52249845, 1ENB*CHGR1B Load Test, reviewed on September 27, 2011
  • WO 00268148, HVK-TS71D Calibration of Low Chill Water Temperature Pretrip, reviewed on September 29, 2011 The inspectors selected these activities based upon the structure, system, or component's ability to affect risk. The inspectors evaluated these activities for the following (as applicable):
  • The effect of testing on the plant had been adequately addressed; testing was adequate for the maintenance performed
  • Acceptance criteria were clear and demonstrated operational readiness; test instrumentation was appropriate

The inspectors evaluated the activities against the technical specifications, the Updated Safety Analysis Report, 10 CFR Part 50 requirements, licensee procedures, and various NRC generic communications to ensure that the test results adequately ensured that the equipment met the licensing basis and design requirements. In addition, the inspectors reviewed corrective action documents associated with postmaintenance tests to determine whether the licensee was identifying problems and entering them in the corrective action program and that the problems were being corrected commensurate with their importance to safety. Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of seven postmaintenance testing inspection samples as defined in Inspection Procedure 71111.19-05.

b.

===.1

Introduction.

=

The inspectors identified a Green, noncited violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, for an inadequate calculation methodology used in determining standby gas treatment system operability.

Findings

Description.

On July 21, 2011, the standby gas treatment filter train B heater failed the monthly surveillance test procedure due to an open electrical connection between a heater element and the mounting stud used to secure the element to the bus bar.

The standby gas treatment systems filter train heaters have a total of nine heater elements, three elements per phase. Station engineering personnel developed engineering change EC-30850, GTS-FLT1B Operation with One Heater Element out of Service, to temporarily remove the failed filter train heater element, and revised the surveillance test calculation method for determining filter train power output with only 8 out of 9 heater elements functioning. Technical Specification 5.5.7e, Ventilation Filter Testing Program, requires that standby gas treatment system filter train B dissipate greater than or equal to 61 kW to maintain air relative humidity less than 70 percent passing through the filter. On July 23, 2011, the filter train B passed the revised test procedure with very small margin, producing 61.43 kW. Humidity greater than 70 percent is considered detrimental to the charcoal filters ability to retain radioactive iodine.

On August 17, 2011, the standby gas treatment filter train B heater failed the monthly surveillance test due to only producing 60.28 kW. Operations declared the system inoperable and actions were taken to repair the defective heater element. The system was returned to full qualification with nine heater elements installed, and passed the monthly surveillance.

The inspectors reviewed the modified calculation methodology for standby gas treatment system heater operability. Neither the surveillance test nor engineering change EC-30850 calculation method accounted for instrument uncertainty when determining the kW output. The inspectors concluded that to have reasonable assurance of operability the calculation should have accounted for instrument uncertainty. The margin between the satisfactory test on July 23, 2011, and the

unsatisfactory test on August 17, 2011, was within the instrument tolerances of the different amp and voltmeters used to measure the filter train heater current and voltage use. In addition, questioning by the inspectors revealed that the calculation had used a nonconservative value for the voltage drop from the heater breaker to the heater.

Analysis.

The failure to have an adequate calculation methodology for the standby gas treatment heater output power is a performance deficiency. The inspectors determined that the performance deficiency was similar to the not minor if statement contained in example 3j of Inspection Manual Chapter 0612, Appendix E, Examples of Minor Issues, because reasonable doubt of system operability existed. Using Inspection Manual Chapter 0612, Appendix B, Issue Screening, the inspectors determined that this finding was more than minor because it was associated with the design control attribute of the Barrier Integrity Cornerstone to maintain radiological barrier functionality of standby gas treatment trains, and affected the cornerstone objective to provide reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents or events. Specifically, operating the standby gas system filter train heaters without sufficient output power is detrimental to the ability of the charcoal filters to retain radioactive iodine. This could result in a greater amount of radiation release to the environment in the event of an accident. In accordance with Inspection manual Chapter 0609, Appendix A, Significance Determination of Reactor Inspection Findings for At-Power Situations, the Phase 1 significance determination process screening determined the finding to be only of very low safety significance (Green) because the finding only represented a degradation of the radiological barrier function provided for the standby gas treatment system. The apparent cause of this finding was the decision to develop an engineering evaluation that did not include instrument uncertainly and did not validate the correct voltage drop between the filter train heater feeder breaker and the heater elements. The cause of this finding has a crosscutting aspect in the area of human performance associated with the decision-making component because station personnel failed to use conservative assumptions when developing the modified output power methodology for operation of the standby gas treatment system filter heaters with only 8 of 9 heater elements installed H.1(b).

Enforcement.

Title 10 CFR Part 50, Appendix B, Criterion III, Design Control requires, in part, that design control measures provide for verifying or checking the adequacy of design, such as by the performance of design reviews, by the use of alternate or simplified calculational methods, or by the performance of suitable testing program.

Contrary to this, on July 23, 2011, the licensees design control measures did not provide for verifying the adequacy of design, in that those measures failed to verify satisfactory performance of the standby gas treatment system due to the failure of station personnel to account for instrument uncertainty in the modified heater output calculation. Because this finding was of very low safety significance and has been entered into the licensees corrective action program as Condition Report CR-RBS-2100-07332, this violation is being treated as a noncited violation consistent with NRC Enforcement Policy: NCV 05000458/2011004-01, Inadequate Standby Gas Treatment Electric Heater Power Output Calculation.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors reviewed the Updated Safety Analysis Report, procedure requirements, and technical specifications to ensure that the surveillance activities listed below demonstrated that the systems, structures, and/or components tested were capable of performing their intended safety functions. The inspectors either witnessed or reviewed test data to verify that the significant surveillance test attributes were adequate to address the following:

  • Preconditioning
  • Evaluation of testing impact on the plant
  • Acceptance criteria
  • Test equipment
  • Procedures
  • Jumper/lifted lead controls
  • Test data
  • Testing frequency and method demonstrated technical specification operability
  • Test equipment removal
  • Restoration of plant systems
  • Fulfillment of ASME Code requirements
  • Updating of performance indicator data
  • Engineering evaluations, root causes, and bases for returning tested systems, structures, and components not meeting the test acceptance criteria were correct
  • Reference setting data

The inspectors also verified that licensee personnel identified and implemented any needed corrective actions associated with the surveillance testing.

  • STP-204-6301, DIV I LPCI (RHR) Pump and Valve Operability Test, performed inservice test sample on July 7, 2011
  • STP-257-4501, RMS Primary Containment Purge Isolation Radiation High Activity Monitor Channel Functional Test (RMS-RE21A), on July 10, 2011
  • STP-309-0603, Division III ECCS Test, performed on July 26, 2011
  • REP-0007, Spent Fuel Pool Coupon Surveillance Program, performed on August 22, 2011
  • STP-204-4510, LPCI Pump C Discharge Flow - Low, Channel Functional Test (E12-N652C), performed on September 13, 2011 Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of five surveillance testing inspection samples as defined in Inspection Procedure 71111.22-05.

b.

No findings were identified.

Findings

1EP6 Drill Evaluation

Emergency Preparedness Drill Observation a.

The inspectors evaluated the conduct of routine licensee emergency drills on July 14, 2011, and August 2, 2011, to identify any weaknesses and deficiencies in classification, notification, and protective action recommendation development activities.

The inspectors observed emergency response operations in the simulator, emergency operations facility, and technical support center to determine whether the event classification, notifications, and protective action recommendations were performed in accordance with procedures. The inspectors also attended the licensee drill critique to compare any inspector-observed weakness with those identified by the licensee staff in order to evaluate the critique and to verify whether the licensee staff was properly identifying weaknesses and entering them into the corrective action program. As part of the inspection, the inspectors reviewed the drill package and other documents listed in the attachment.

Inspection Scope

These activities constitute completion of two samples as defined in Inspection Procedure 71114.06-05.

b.

No findings were identified.

Findings

RADIATION SAFETY

Cornerstone: Occupational and Public Radiation Safety

2RS0 6 Radioactive Gaseous and Liquid Effluent Treatment

a. Inspection Scope

This area was inspected to:

(1) ensure the gaseous and liquid effluent processing systems are maintained so radiological discharges are properly mitigated, monitored, and evaluated with respect to public exposure;
(2) ensure abnormal radioactive gaseous or liquid discharges and conditions, when effluent radiation monitors are out-of-service, are controlled in accordance with the applicable regulatory requirements and licensee procedures;
(3) verify the licensee=s quality control program ensures the radioactive effluent sampling and analysis requirements are satisfied so discharges of radioactive materials are adequately quantified and evaluated; and
(4) verify the adequacy of public dose projections resulting from radioactive effluent discharges. The inspectors used the requirements in 10 CFR Part 20; 10 CFR Part 50, Appendices A and I; 40 CFR Part 190; the Offsite Dose Calculation Manual, and licensee procedures required by the Technical Specifications as criteria for determining compliance. The inspectors interviewed licensee personnel and reviewed and/or observed the following items:
  • Radiological effluent release reports since the previous inspection and reports related to the effluent program issued since the previous inspection, if any
  • Effluent program implementing procedures, including sampling, monitor setpoint determinations and dose calculations
  • Equipment configuration and flow paths of selected gaseous and liquid discharge system components, filtered ventilation system material condition, and significant changes to their effluent release points, if any, and associated 10 CFR 50.59 reviews
  • Selected portions of the routine processing and discharge of radioactive gaseous and liquid effluents (including sample collection and analysis)
  • Controls used to ensure representative sampling and appropriate compensatory sampling
  • Results of the inter-laboratory comparison program
  • Effluent stack flow rates
  • Surveillance test results of technical specification-required ventilation effluent discharge systems since the previous inspection
  • Significant changes in reported dose values, if any
  • A selection of radioactive liquid and gaseous waste discharge permits
  • Part 61 analyses and methods used to determine which isotopes are included in the source term
  • Meteorological dispersion and deposition factors
  • Latest land use census
  • Records of abnormal gaseous or liquid tank discharges, if any
  • Groundwater monitoring results
  • Changes to the licensees written program for indentifying and controlling contaminated spills/leaks to groundwater, if any
  • Identified leakage or spill events and entries made into 10 CFR 50.75 (g)records, if any, and associated evaluations of the extent of the contamination and the radiological source term
  • Offsite notifications and reports of events associated with spills, leaks, or groundwater monitoring results, if any
  • Audits, self-assessments, reports, and corrective action documents related to radioactive gaseous and liquid effluent treatment since the last inspection

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of the one required sample, as defined in Inspection Procedure 71124.06-05.

b. Findings

No findings were identified.

2RS0 7 Radiological Environmental Monitoring Program

a. Inspection Scope

This area was inspected to:

(1) ensure that the radiological environmental monitoring program verifies the impact of radioactive effluent releases to the environment and sufficiently validates the integrity of the radioactive gaseous and liquid effluent release program;
(2) verify that the radiological environmental monitoring program is implemented consistent with the licensees technical specifications and/or offsite dose

calculation manual, and to validate that the radioactive effluent release program meets the design objective contained in Appendix I to 10 CFR Part 50; and

(3) ensure that the radiological environmental monitoring program monitors non-effluent exposure pathways, is based on sound principles and assumptions, and validates that doses to members of the public are within the dose limits of 10 CFR Part 20 and 40 CFR Part 190, as applicable. The inspectors reviewed and/or observed the following items:
  • Selected air sampling and thermoluminescence dosimeter monitoring stations
  • Collection and preparation of environmental samples
  • Operability, calibration, and maintenance of meteorological instruments
  • Selected events documented in the annual environmental monitoring report which involved a missed sample, inoperable sampler, lost thermoluminescence dosimeter, or anomalous measurement
  • Selected structures, systems, or components that may contain licensed material and has a credible mechanism for licensed material to reach ground water
  • Significant changes made by the licensee to the offsite dose calculation manual as the result of changes to the land census or sampler station modifications since the last inspection
  • Calibration and maintenance records for selected air samplers, composite water samplers, and environmental sample radiation measurement instrumentation
  • Interlaboratory comparison program results
  • Audits, self-assessments, reports, and corrective action documents related to the radiological environmental monitoring program since the last inspection

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of the one required sample as defined in Inspection Procedure 71124.07-05.

b. Findings

No findings were identified.

2RS08 Radioactive Solid Waste Processing, and Radioactive Material Handling, Storage, and Transportation (71124.08)

a. Inspection Scope

This area was inspected to verify the effectiveness of the licensee=s programs for processing, handling, storage, and transportation of radioactive material. The inspectors used the requirements of 10 CFR Parts 20, 61, and 71 and Department of Transportation regulations contained in 49 CFR Parts 171-180 for determining compliance. The inspectors interviewed licensee personnel and reviewed the following items:

  • The solid radioactive waste system description, process control program, and the scope of the licensee=s audit program
  • Control of radioactive waste storage areas including container labeling/marking and monitoring containers for deformation or signs of waste decomposition
  • Changes to the liquid and solid waste processing system configuration including a review of waste processing equipment that is not operational or abandoned in place
  • Radio-chemical sample analysis results for radioactive waste streams and use of scaling factors and calculations to account for difficult-to-measure radionuclides
  • Processes for waste classification including use of scaling factors and 10 CFR Part 61 analysis
  • Shipment packaging, surveying, labeling, marking, placarding, vehicle checking, driver instructing, and preparation of the disposal manifest
  • Audits, self-assessments, reports, and corrective action reports radioactive solid waste processing, and radioactive material handling, storage, and transportation performed since the last inspection

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of the one required sample as defined in Inspection Procedure 71124.08-05.

b. Findings

No findings were identified.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification

.1 Data Submission Issue

a.

The inspectors performed a review of the performance indicator data submitted by the licensee for the second quarter 2011 performance indicators for any obvious inconsistencies prior to its public release in accordance with Inspection Manual Chapter 0608, Performance Indicator Program.

Inspection Scope

This review was performed as part of the inspectors normal plant status activities and, as such, did not constitute a separate inspection sample.

b.

No findings were identified.

Findings

.2 Mitigating Systems Performance Index - Heat Removal System (MS08)

a.

The inspectors sampled licensee submittals for the mitigating systems performance index - heat removal system performance indicator for the period from the third quarter 2010 through the second quarter 2011. To determine the accuracy of the performance indicator data reported during those periods, the inspectors used definitions and guidance contained in NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6. The inspectors reviewed the licensees operator narrative logs, issue reports, event reports, mitigating systems performance index derivation reports, and NRC integrated inspection reports for the period of July 2010 through June 2011 to validate the accuracy of the submittals. The inspectors reviewed the mitigating systems performance index component risk coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the performance indicator data collected or transmitted for this indicator and none were identified. Specific documents reviewed are described in the attachment to this report.

Inspection Scope

These activities constitute completion of one mitigating systems performance index - heat removal system sample as defined in Inspection Procedure 71151-05.

b.

No findings were identified.

Findings

.3 Mitigating Systems Performance Index - Residual Heat Removal System (MS09)

a.

The inspectors sampled licensee submittals for the mitigating systems performance index - residual heat removal system performance indicator for the period from the third quarter 2010 through the second quarter 2011. To determine the accuracy of the performance indicator data reported during those periods, the inspectors used definitions and guidance contained in NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6. The inspectors reviewed the licensees operator narrative logs, issue reports, mitigating systems performance index derivation reports, event reports, and NRC integrated inspection reports for the period of July 2010 through June 2011 to validate the accuracy of the submittals. The inspectors reviewed the mitigating systems performance index component risk coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the performance indicator data collected or transmitted for this indicator and none were identified. Specific documents reviewed are described in the attachment to this report.

Inspection Scope

These activities constitute completion of one mitigating systems performance index - residual heat removal system sample as defined in Inspection Procedure 71151-05.

b.

No findings were identified.

Findings

.4 Mitigating Systems Performance Index - Cooling Water Systems (MS10)

a.

The inspectors sampled licensee submittals for the mitigating systems performance index - cooling water systems performance indicator for the period from the third quarter 2010 through the second quarter 2011. To determine the accuracy of the performance indicator data reported during those periods, the inspectors used definitions and guidance contained in NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6. The inspectors reviewed the licensees operator narrative logs, issue reports, mitigating systems performance index derivation reports, event reports, and NRC integrated inspection reports for the period of July 2010 through June 2011 to validate the accuracy of the submittals. The inspectors reviewed the mitigating systems performance index component risk coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the performance indicator data collected or transmitted for this indicator and none were identified. Specific documents reviewed are described in the attachment to this report.

Inspection Scope

These activities constitute completion of one mitigating systems performance index - cooling water system sample as defined in Inspection Procedure 71151-05.

b.

No findings were identified.

Findings

4OA2 Identification and Resolution of Problems

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical Protection

.1 Routine Review of Identification and Resolution of Problems

a.

As part of the various baseline inspection procedures discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that they were being entered into the licensees corrective action program at an appropriate threshold, that adequate attention was being given to timely corrective actions, and that adverse trends were identified and addressed. The inspectors reviewed attributes that included the complete and accurate identification of the problem; the timely correction, commensurate with the safety significance; the evaluation and disposition of performance issues, generic implications, common causes, contributing factors, root causes, extent of condition reviews, and previous occurrences reviews; and the classification, prioritization, focus, and timeliness of corrective actions. Minor issues entered into the licensees corrective action program because of the inspectors observations are included in the attached list of documents reviewed.

Inspection Scope

These routine reviews for the identification and resolution of problems did not constitute any additional inspection samples. Instead, by procedure, they were considered an integral part of the inspections performed during the quarter and documented in Section 1 of this report.

b.

No findings were identified.

Findings

.2 Daily Corrective Action Program Reviews

a.

In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of Inspection Scope

items entered into the licensees corrective action program. The inspectors accomplished this through review of the stations daily corrective action documents.

The inspectors performed these daily reviews as part of their daily plant status monitoring activities and, as such, did not constitute any separate inspection samples.

b.

No findings were identified.

Findings

.3 Selected Issue Follow-up Inspection

a.

During a review of items entered in the licensees corrective action program, the inspectors recognized a corrective action item documenting an event involving a downpower due to a steam leak on a main steam equalizing header drain. The inspectors discussed the event with licensee management, engineering, operations, and maintenance personnel to understand the event and the scope of the corrective actions taken by the licensee.

Inspection Scope

These activities constitute completion of one in-depth problem identification and resolution sample as defined in Inspection Procedure 71152-05.

b.

Introduction.

The inspectors identified a self-revealing, Green finding involving inadequate corrective actions in response to a failure in the main steam equalizing header drain bypass valve, resulting in a steam leak and an unplanned plant down power.

Findings

Description.

On February 12, 2011, during plant start-up from refuel outage 16, plant operators discovered that the main steam equalizing header drain bypass valve had dual position indication instead of closed. This information was reported to the outage control center. Based on previous maintenance during the outage and operation of the valve earlier in the plant start-up, the outage control center and main control room personnel presumed the dual position indication was an indication only issue and the actual valve position was closed as intended. Station management failed to take adequate follow-up actions to ensure the valve was in the closed position, and also failed to address the potential consequences of normal power operations with the valve partially open.

On June 19, 2011, plant operators in the turbine building identified a large steam leak near the condenser. Operators reduced station power to approximately 40 percent in order to facilitate identification of the leak. During the investigation, station personnel found that the main steam equalizing header drain piping developed a through wall leak beyond the bypass valve. The valve had not been in the closed position and was partially open. Consequently, fluid flow through the valve increased, causing water to

flash to steam due to the large pressure drop near the condenser resulting in accelerated pipe wall erosion and piping failure. Station personnel isolated the damaged steam drain piping and returned the plant to full power.

Corrective actions included plans to develop and implement a comprehensive program that establishes nuclear safety culture as the overriding station priority; perform a needs analysis to determine training requirements related to the importance of aggressively pursuing the satisfactory resolution of abnormal conditions (e.g., this condition where a valve dual position indication was not verified by other means as correct); troubleshoot the valve during refueling outage 17 to determine why the valve failed to close; evaluate the piping failure mechanism to incorporate the findings into flow accelerated corrosion program as needed; and replace any damage piping during refueling outage 17.

Analysis.

The failure to ensure that the corrective action process properly addressed the dual indication on the bypass valve during plant start-up was a performance deficiency.

Specifically, EN-LI-102, "Corrective Action Process," states that individuals are required to take immediate actions to resolve adverse conditions to minimize the consequence of the condition. Contrary to this, during refuelling outage 16, the outage control center and main control room personnel failed to adequately investigate the dual indications identified on the main steam equalizing header drain bypass valve. The finding was more than minor because it was associated with the equipment performance attribute of the initiating events cornerstone and affected the cornerstone objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. The inspectors reviewed the finding using Inspection Manual Chapter 0609, Appendix A, Significance Determination of Reactor Inspection Findings for At-Power Situations. Based on the Phase 1 screening of the finding, the inspectors determined that the finding was of very low safety significance (Green) because it was not a loss of coolant accident initiator, did not contribute to both the likelihood of an initiating event and the likelihood that mitigating equipment or functions would not be available, nor increase the likelihood of an external event (seismic, flooding, or severe weather event). The apparent cause of the performance deficiency was that the control room and outage control center personnel presumed that the main control room dual indication for the valve was incorrect because previously valve operation successfully closed the valve. Consequently, this finding has a crosscutting aspect in the area of human performance associated with the decision-making component because station personnel failed to use a systematic process to assess the condition of the bypass valve, and failed to verify the validity of the underlying assumptions that were used to justify operation with the valve having dual indication

H.1(a).

Enforcement.

Enforcement action does not apply because the performance deficiency did not violate regulatory requirements. Because this finding does not involve a violation of regulatory requirements and has very low safety significance, it is characterized as a finding and is designated as FIN 05000458/2011004-02, Ineffective Corrective Actions on the Main Steam Equalizing Header Drain Bypass Valve Results in an Unplanned Down Power.

.4 Selected Issue Follow-up Inspection

a.

During a review of items entered in the licensees corrective action program, the inspectors recognized a corrective action item documenting a human performance error involving an operator performing maintenance on the emergency diesel generator without a work order. The inspectors discussed the event with licensee management, engineering, and operations to understand the human performance error and the scope of the corrective actions taken by the licensee. The inspectors determined that the error was a minor violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, for performing maintenance on the emergency diesel generator lube oil strainer without appropriate work instructions.

Inspection Scope

These activities constitute completion of one in-depth problem identification and resolution sample as defined in Inspection Procedure 71152-05.

b.

No findings were identified.

Findings

.5 Selected Issue Follow-up Inspection

a.

During a review of items entered in the licensees corrective action program, the inspectors recognized a corrective action item documenting multiple human performance errors involving a misalignment of the reactor water cleanup system. The inspectors discussed the event with licensee management and operations to understand the human performance errors and the scope of the corrective actions taken by the licensee. The inspectors determined that the error was a minor violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, for failure to follow procedure.

Inspection Scope

These activities constitute completion of one in-depth problem identification and resolution sample as defined in Inspection Procedure 71152-05.

b.

No findings were identified.

Findings

4OA6 Meetings

Exit Meeting Summary

On September 16, 2011, the inspectors presented the results of the radiation safety inspections to Mr. E. Olson, Site Vice President, and other members of the licensee staff. The licensee acknowledged the issues presented. The inspectors asked the licensee whether any materials

examined during the inspection should be considered proprietary. No proprietary information was identified.

On October 12, 2011, the inspectors presented the integrated inspection results to Mr. E. Olson, Site Vice President, and other members of the licensee staff. The licensee acknowledged the issues presented. The inspector asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.

4OA7 Licensee-Identified Violations

The following violations of very low safety significance (Green) were identified by the licensee and are violations of NRC requirements which meet the criteria of Section 2.3.2 of the NRC Enforcement Policy for being dispositioned as noncited violations:

.1 Title 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, states, in part, that

measures shall be established to assure that conditions adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and equipment, and nonconformances are promptly identified and corrected. Contrary to these requirements, the licensee took incomplete measures to ensure the completion of slow turbine rolls to remediate the air voiding in the lube oil system of the reactor core isolation cooling turbine. On April 17, 2010, operations reported a low oil level in both sight glasses of the reactor core isolation cooling turbine. The investigation attributed the cause of the low oil level as a failure to perform a slow roll on the reactor core isolation cooling turbine following system maintenance. On February 10, 2011, during the plant start-up from refueling outage 17, station management canceled the work order to perform the slow roll of the reactor core isolation cooling turbine following lube oil system maintenance, resulting in air accumulating in the lube oil system. The finding was considered to be of very low safety significance (Green) because it was not a design or qualification deficiency; did not represent either a loss of system safety function, an actual loss of safety function of a single train, or an actual loss of safety function; and did not screen as potentially risk significant due to a seismic, flooding, or severe weather initiating event. The issue has been entered into the licensees corrective action program as Condition Report CR-RBS-2010-03854.

.2 Technical Specification 5.4.1 requires that written procedures shall be established,

implemented, and maintained covering, in part, the applicable procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978. In RG 1.33, section 9 of Appendix A says, in part, that maintenance that can affect the performance of safety-related equipment should be performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances. Contrary to the above, between February 4, 2011, and February 7, 2011 the licensee performed maintenance that could affect the performance of safety-related equipment in accordance with documented instructions that were not appropriate to the circumstances, in that:

  • Removing temporary filter media installed in safety-related unit coolers was maintenance that could affect the performance of safety-related equipment.
  • Removal of filter media was performed in accordance with task 02 of work order 230363.
  • Although task 02 of work order 230363 identified the unit coolers from which filter media were to be removed, task 02 of work order 230363 did not include details that described behind which unit cooler door the media were located. It also did not include criteria for determining that the media had been successfully removed.

As a result, on March 3, 2011, a worker assigned to verify that filter media had been removed from safety-related unit coolers via task 02 of work order 230363 failed to locate the installed filter media and signed off on the work order to indicate that the media had been removed. This issue is addressed in the licensees corrective action program in Condition Report CR-RBS-2010-04331.

.3 Technical Specification 5.4.1 requires that written procedures shall be established,

implemented, and maintained covering, in part, the applicable procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978. In RG 1.33, section 9 of Appendix A says, in part, that maintenance that can affect the performance of safety-related equipment should be performed in accordance with written procedures appropriate to the circumstances. EN-WM-102, Work Implementation and Closeout, constituted documented instructions that were appropriate to the circumstances of performing maintenance that could affect the performance of safety-related equipment.

Removing temporary filter media from various unit coolers as described in task 02 of work order 230363 was maintenance that could affect the performance of safety-related equipment. Contrary to the above, on February 7, 2011, before workers had completed task 02 of work order 230363, a Supervisor/Lead Worker set the status of that task to FINISHED within the work-control database without reviewing the associated task paperwork for signoffs/signatures. As a result, task 02 of work order 230363 was not completed, and temporary filter media remained in several unit coolers as the licensee started up the plant and returned it to full power. This issue is addressed in the licensees corrective action program in Condition Report CR-RBS-2010-04331.

.4 Technical Specification 5.4.1 requires that written procedures shall be established,

implemented, and maintained covering, in part, the applicable procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978. In RG 1.33, section 9 of Appendix A says, in part, that maintenance that can affect the performance of safety-related equipment should be performed in accordance with written procedures appropriate to the circumstances. Procedure EN-MA-101, Fundamentals of Maintenance, Rev. 9, in part, requires workers to place the equipment being worked on in a safe condition and contact their supervisor if any unexpected condition, event or results occur during the performance of the job. It also requires the worker to initiate a corresponding Condition Report. Contrary to the above, on March 3, 2011, after the licensee had discovered that not all signatures had been entered into task 02 of work order 230363 and a Mechanical Maintenance worker had been assigned to verify that the filter media installed under task 01 of work order 230363 had been removed, an unexpected condition occurred, in that although task 02 of work order 230363 indicated that some filter media were still installed, the worker found no filter media where he looked. When this occurred, that worker did not contact his supervisor and did not

initiate a condition report. Instead, the worker signed task 02 of work order 230363 to indicate that the media had been removed. As a result, temporary filter media that should have been but were not removed via that task at the end of the refueling outage remained in several unit coolers as the plant operated at full power. This issue is addressed in the licensees corrective action program in Condition Report CR-RBS-2010-04331.

.5 Title 10 CFR 50 Appendix B, Criterion XVI, Corrective Action, states, in part, that

measures shall be established to assure that conditions adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and equipment, and nonconformances are promptly identified and corrected. Contrary to these requirements, plant personnel failed to properly evaluate and correct a damaged temperature control valve on the Division II emergency diesel generator jacket water system. During maintenance on the valve, the valve bonnet assembly fell approximately three feet from the top of the work table to the concrete floor causing a bend in the valve crank frame, which is a non-pressure retaining part. A condition report documented the damage, but station management failed to perform a formal assessment or a use as-is evaluation before installing the damaged pressure control valve bonnet assembly back into the valve body on the Division II emergency diesel generator. The finding is considered to be of very low safety significance (Green), because it was not a design or qualification deficiency; did not represent either a loss of system safety function, an actual loss of safety function of a single train, or an actual loss of safety function; and did not screen as potentially risk significant due to a seismic, flooding, or severe weather initiating event. The issue has been entered into the licensees corrective action program as condition report CR-RBS-2010-04785.

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

D. Burnett, Manager, Emergency Preparedness
G. Bush, Manager, Material, Procurement, and Contracts
M. Chase, Manager, Training
W. Chatterton, Sr. Lead Technical Specialist, Program & Components Engineering
H. Choate, Engineer, System Engineering
J. Clark, Manager, Licensing
L. Coats, Senior Health Physicist/Chemistry Specialist
C. Colman, Manager, Engineering Programs & Components
F. Corley, Manager, Design Engineering
R. Creel, Superintendent, Plant Security
M. Feltner, Manager, Planning and Scheduling, Outages
C. Forpahl, Manager, System Engineering
A. Fredieu, Manager, Outage
W. Fountain, Senior Licensing Specialist
R. Gadbois, General Manager, Plant Operations
T. Gates, Assistant Operations Manager - Shift
H. Goodman, Director, Engineering
D. Heath, Supervisor, Radiation Protection
R. Heath, Manager, Chemistry
K. Huffstatler, Senior Licensing Specialist
L. Kitchen, Manager, Maintenance
G. Krause, Assistant Operations Manager - Support
E. Olson, Site Vice President
R. Persons, Superintendent, Training
G. Pierce, Manager, Radiation Protection
J. Roberts, Director, Nuclear Safety Assurance
J. Schlesinger, Senior Engineer, Design Engineering
T. Shenk, Assistant Operations Manager - Training
W. Spell, Senior Health Physicist/Chemistry Specialist
M. Spustack, Supervisor, Engineering
J. Standridge, Planner, Emergency Preparedness
N. Tison, Planner, Emergency Preparedness
D. Vines, Manager, Corrective Actions and Assessments
J. Vukovics, Supervisor, Reactor Engineering
J. Wilson, Supervisor, System Engineering
L. Woods, Manager, Quality Assurance
S. Zabaski, Senior Health Physicist/Chemistry Specialist

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000458/2011004-01 NCV Inadequate Standby Gas Treatment Electric Heater Power Output Calculation
05000458/2011004-02 FIN Ineffective Corrective Actions on the Main Steam Equalizing Header Drain Bypass Valve Results in an Unplanned Down Power

LIST OF DOCUMENTS REVIEWED