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| issue date = 08/12/2015
| issue date = 08/12/2015
| title = IR 05000219/2015002, April 1, 2015 - June 30, 2015, Oyster Creek Nuclear Generating Station, Integrated Inspection Report
| title = IR 05000219/2015002, April 1, 2015 - June 30, 2015, Oyster Creek Nuclear Generating Station, Integrated Inspection Report
| author name = Kennedy S R
| author name = Kennedy S
| author affiliation = NRC/RGN-I/DRP/PB6
| author affiliation = NRC/RGN-I/DRP/PB6
| addressee name = Hanson B
| addressee name = Hanson B
Line 24: Line 24:


==Dear Mr. Hanson:==
==Dear Mr. Hanson:==
On June 30, 2015, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Oyster Creek Nuclear Generating Station. The enclosed inspection report documents the inspection results, which were discussed on July 10, 2015, with Mr. G. Stathes, Site Vice President, and other members of your staff. NRC inspectors examined activities conducted under your license as they relate to safety and se. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. The inspectors documented four findings of very low safety significance (Green) in this report. One finding involved a violation of NRC requirements. Because of the very low safety significance, and because they are entered into your corrective action program, the NRC is treating these findings as non-cited violations, consistent with Section 2.3.2.a of the NRC Enforcement Policy. If you contest the non-cited violations in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at Oyster Creek Nuclear Generating Station. In addition, if you disagree with the cross-cutting aspect assigned to any finding, or a finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region I, and the NRC Resident Inspector at Oyster Creek Nuclear Generating Station. In accordance with Title 10 of the Code of Federal Regulations py of this letter, its enclosure, and your response (if any) will be Management System (ADAMS). ADAMS is accessible from the NRC website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
On June 30, 2015, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Oyster Creek Nuclear Generating Station. The enclosed inspection report documents the inspection results, which were discussed on July 10, 2015, with Mr. G. Stathes, Site Vice President, and other members of your staff.
 
NRC inspectors examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.
 
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
 
The inspectors documented four findings of very low safety significance (Green) in this report.
 
One finding involved a violation of NRC requirements. Because of the very low safety significance, and because they are entered into your corrective action program, the NRC is treating these findings as non-cited violations, consistent with Section 2.3.2.a of the NRC Enforcement Policy.
 
If you contest the non-cited violations in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at Oyster Creek Nuclear Generating Station. In addition, if you disagree with the cross-cutting aspect assigned to any finding, or a finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region I, and the NRC Resident Inspector at Oyster Creek Nuclear Generating Station. In accordance with Title 10 of the Code of Federal Regulations (CFR) 2.390 of the NRCs Rules of Practice, a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRCs Public Document Room or from the Publicly Available Records component of the NRCs Agencywide Documents Access Management System (ADAMS). ADAMS is accessible from the NRC website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).


Sincerely,
Sincerely,
/RA/ Silas R. Kennedy, Chief Reactor Projects Branch 6 Division of Reactor Projects Docket Nos. 50-219 License Nos. DPR-16 Enclosure: Inspection Report 05000219/2015002 w/Attachment: Supplementary Information cc w/encl: Distribution via ListServ
/RA/  
 
Silas R. Kennedy, Chief Reactor Projects Branch 6 Division of Reactor Projects  
 
Docket Nos. 50-219 License Nos. DPR-16  


ML15224B475  SUNSI Review Non-Sensitive Sensitive Publicly Available Non-Publicly Available OFFICE RI/DRP RI/DRP RI/DRP NAME APatel/ SRK for AZiedonis/ AVZ SKennedy/ SRK DATE 08/12 /15 08/ 12 /15 08/ 12 /15 1 Enclosure U.S. NUCLEAR REGULATORY COMMISSION REGION I Docket Nos.: 50-219 License Nos.: DPR-16 Report No.: 05000219/2015002 Licensee: Exelon Nuclear Facility: Oyster Creek Nuclear Generating Station Location: Forked River, New Jersey Dates: April 1, 2015 June 30, 2015 Inspectors: A. Patel, Senior Resident Inspector E. Andrews, Resident Inspector B. Dionne, Health Physicist S. Elkhiamy, Project Engineer T. Fish, Senior Operations Examiner M. Patel, Operations Examiner Approved By: Silas R. Kennedy, Chief Reactor Projects Branch 6 Division of Reactor Projects 2
===Enclosure:===
Inspection Report 05000219/2015002 w/Attachment: Supplementary Information
 
REGION I==
Docket Nos.:
50-219  
 
License Nos.:
DPR-16  
 
Report No.:  
 
05000219/2015002  
 
Licensee:  
 
Exelon Nuclear  
 
Facility:  
 
Oyster Creek Nuclear Generating Station  
 
Location:  
 
Forked River, New Jersey  
 
Dates:  
 
April 1, 2015 - June 30, 2015  
 
Inspectors:  
 
A. Patel, Senior Resident Inspector E. Andrews, Resident Inspector B. Dionne, Health Physicist S. Elkhiamy, Project Engineer T. Fish, Senior Operations Examiner M. Patel, Operations Examiner  
 
Approved By:
Silas R. Kennedy, Chief  
 
Reactor Projects Branch 6  
 
Division of Reactor Projects  


=SUMMARY OF FINDINGS=
=SUMMARY OF FINDINGS=
IR 05000219/2015002; 04/01/2015 06/30/2015; Exelon Energy Company, LLC, Oyster Creek Generating Station; Internal Flooding, Licensed Operator Requalification Program, Follow-Up of Events. This report covered a three-month period of inspection by resident inspectors and announced inspections performed by regional inspectors. One NRC-identified finding and two self-revealing findings of very low safety significance (Green) were identified during this inspection. Additionally, a self-revealing non-cited violation (NCV) of very low safety significance (Green) was also documented in this report. The significance of most findings is indicated by their color , dated April 29, 2015. The cross-cutting aspects for the findings Aspects Within Cross-Cutting Areas, dated December 4, Enforcement Policy, dated February 4, 2015. operation of commercial nuclear power reactors is described in NUREG-5.
IR 05000219/2015002; 04/01/2015 - 06/30/2015; Exelon Energy Company, LLC, Oyster Creek  
 
Generating Station; Internal Flooding, Licensed Operator Requalification Program, Follow-Up of Events.
 
This report covered a three-month period of inspection by resident inspectors and announced inspections performed by regional inspectors. One NRC-identified finding and two self-revealing findings of very low safety significance (Green) were identified during this inspection.
 
Additionally, a self-revealing non-cited violation (NCV) of very low safety significance (Green)was also documented in this report. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP), dated April 29, 2015. The cross-cutting aspects for the findings were determined using IMC 0310, Aspects Within Cross-Cutting Areas, dated December 4, 2014. All violations of NRC requirements are dispositioned in accordance with the NRCs Enforcement Policy, dated February 4, 2015. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 5.


===Cornerstone: Initiating Events===
===Cornerstone: Initiating Events===
: '''Green.'''
: '''Green.'''
A self-revealing NCV of Technical Specification because Exelon did not during startup from a forced outage (1F36), Exelon did not follow procedure 303, which required correct valve lineups for system restoration of reactor water cleanup (RWCU) after system isolation. This resulted in decreasing reactor water level, which was automatically terminated by a second RWCU isolation. Exelon entered this issue into the corrective action program. Planned corrective actions include enhancing operator training in system knowledge and procedure compliance and revising startup procedures. This finding is determined to be more than minor because it is associated with the human performance attribute of the Initiating Events cornerstone and affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, Exelon did not properly lineup the RWCU system after isolation, which resulted in a water level transient and challenging the critical safety function of inventory control. This finding is determined to be of very low safety significance (Green), because it did not cause a reactor trip and the loss of mitigation equipment relied upon to transition the plant from the onset of the trip to a stable shutdown condition. This finding has a cross-cutting aspect in the area of Human Performance, Challenge the Unknown, because Exelon did not recognize and plan for the possibility of mistakes, or implement appropriate error reduction tools. Specifically, the operators did not stop and fully communicate plant condition after the initial RWCU isolation. Consequently, operators opened the RWCU system inlet valve due to the increasing water level without following procedure guidance. [H.11] (Section 4OA3)
A self-revealing NCV of Technical Specification 6.8.1(a), Procedures and Programs, was identified because Exelon did not follow procedure 303, Reactor Cleanup Demineralizer System, during the system restoration on March 26, 2015. Specifically, during startup from a forced outage (1F36), Exelon did not follow procedure 303, which required correct valve lineups for system restoration of reactor water cleanup (RWCU) after system isolation. This resulted in decreasing reactor water level, which was automatically terminated by a second RWCU isolation. Exelon entered this issue into the corrective action program. Planned corrective actions include enhancing operator training in system knowledge and procedure compliance and revising startup procedures.
 
This finding is determined to be more than minor because it is associated with the human performance attribute of the Initiating Events cornerstone and affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, Exelon did not properly lineup the RWCU system after isolation, which resulted in a water level transient and challenging the critical safety function of inventory control. This finding is determined to be of very low safety significance (Green), because it did not cause a reactor trip and the loss of mitigation equipment relied upon to transition the plant from the onset of the trip to a stable shutdown condition. This finding has a cross-cutting aspect in the area of Human Performance, Challenge the Unknown, because Exelon did not recognize and plan for the possibility of mistakes, or implement appropriate error reduction tools. Specifically, the operators did not stop and fully communicate plant condition after the initial RWCU isolation.
 
Consequently, operators opened the RWCU system inlet valve due to the increasing water level without following procedure guidance. [H.11] (Section 4OA3)
: '''Green.'''
: '''Green.'''
A self-revealing finding was identified because Exelon did not properly screen work in accordance with MA-AA-716-September 12, 2014, Exelon did not screen the human machine interface (HMI) post-maintenance test per the maintenance planning procedure. As a result, on October 12, 2014, Exelon personnel performing the post-maintenance test did not have a work order, which would have included plant configurations and limitations associated with the test. This led to an automatic reactor scram. Exelon entered this issue into the corrective action program. Planned corrective actions include reinforcing with work planners that a work order is required for similar work activities. This finding was determined to be more than minor because it is associated with the human performance attribute of the Initiating Events cornerstone and affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during plant operation. Specifically, resetting the three AVR controllers caused an automatic plant scram. This finding is determined to be of very low safety significance (Green), because it did not cause a reactor trip and the loss of mitigation equipment relied upon to transition the plant from the onset of the trip to a stable shutdown condition. This finding has a cross-cutting aspect in the area of Human Performance, Challenge the Unknown, because Exelon did not recognize and plan for the possibility of mistakes, or implement appropriate error reduction tools. Specifically, on October 12, 2014, Exelon personnel did not stop when faced with the uncertain situation of the HMI screen that did not respond as expected. [H.11] (Section 4OA3)
A self-revealing finding was identified because Exelon did not properly screen work in accordance with MA-AA-716-010, Maintenance Planning. Specifically, on September 12, 2014, Exelon did not screen the automatic voltage regulators (AVR) human machine interface (HMI) post-maintenance test per the maintenance planning procedure.
 
As a result, on October 12, 2014, Exelon personnel performing the post-maintenance test did not have a work order, which would have included plant configurations and limitations associated with the test. This led to an automatic reactor scram. Exelon entered this issue into the corrective action program. Planned corrective actions include reinforcing with work planners that a work order is required for similar work activities.
 
This finding was determined to be more than minor because it is associated with the human performance attribute of the Initiating Events cornerstone and affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during plant operation. Specifically, resetting the three AVR controllers caused an automatic plant scram. This finding is determined to be of very low safety significance (Green), because it did not cause a reactor trip and the loss of mitigation equipment relied upon to transition the plant from the onset of the trip to a stable shutdown condition. This finding has a cross-cutting aspect in the area of Human Performance, Challenge the Unknown, because Exelon did not recognize and plan for the possibility of mistakes, or implement appropriate error reduction tools. Specifically, on October 12, 2014, Exelon personnel did not stop when faced with the uncertain situation of the HMI screen that did not respond as expected. [H.11] (Section 4OA3)  


===Cornerstone: Mitigating Systems===
===Cornerstone: Mitigating Systems===
: '''Green.'''
: '''Green.'''
The inspectors identified a finding associated with Exelon procedure, OP-AA-108-115, Operability Determinations, because Exelon did not adequately assess a degraded floor gasket for the 4 kilovolt (kV) switchgear roll-up door. Specifically, Exelon did not adequately assess the flood and fire functionality of the degraded gasket, which is credited to provide protection to safety-related V switchgear during a postulated internal flood event and to contain the carbon dioxide (CO2) gaseous suppression system during a postulated fire within the   Exelon entered this issue into the corrective action program. Planned corrective actions include reinforcing the operability determination procedure and enhancing operator training in fire and flood functionality of gaskets. Additional corrective actions included repairing the gasket and performing a detailed analysis of the ability of degraded gasket to meet its flooding and fire function. This finding is more than minor because it is associated with the protection against external factors attribute of the Mitigating Systems cornerstone, and affected the cornerstone objective of ensuring the reliability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the degraded floor gasket could have resulted in increased water level in the V switchgear room during a postulated internal flood due to a fire water pipe rupture, therefore affecting the reliability of the 4k switchgear to perform its safety function. In addition, the degraded floor gasket could have resulted in CO2 postulated fire in that switchgear gaseous suppression system to perform its safety function. The inspectors determined that this finding is of very low safety significance (Green) because it is a deficiency that affected the design or qualification of a mitigating structure, system, or component (SSC), where the SSC maintained its operability or functionality. This finding has a cross-cutting aspect in the area of Problem Identification and Resolution, Evaluation, because Exelon did not thoroughly evaluate issues to ensure that resolutions address the causes and extent of conditions commensurate with their safety significance. Specifically, Exelon staff did not thoroughly evaluate the issue associated with the degraded floor gasket for fire and flood functionality. [P.2] (Section 1R06)5
The inspectors identified a finding associated with Exelon procedure, OP-AA-108-115, Operability Determinations, because Exelon did not adequately assess a degraded floor gasket for the D emergency 4 kilovolt (kV) switchgear roll-up door. Specifically,
Exelon did not adequately assess the flood and fire functionality of the degraded gasket, which is credited to provide protection to safety-related D emergency 4kV switchgear during a postulated internal flood event and to contain the carbon dioxide (CO2) gaseous suppression system during a postulated fire within the D switchgear room. Exelon entered this issue into the corrective action program. Planned corrective actions include reinforcing the operability determination procedure and enhancing operator training in fire and flood functionality of gaskets. Additional corrective actions included repairing the gasket and performing a detailed analysis of the ability of degraded gasket to meet its flooding and fire function.
 
This finding is more than minor because it is associated with the protection against external factors attribute of the Mitigating Systems cornerstone, and affected the cornerstone objective of ensuring the reliability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the degraded floor gasket could have resulted in increased water level in the D emergency 4kV switchgear room during a postulated internal flood due to a fire water pipe rupture, therefore affecting the reliability of the D emergency 4k switchgear to perform its safety function. In addition, the degraded floor gasket could have resulted in CO2 leakage out of the D emergency 4k switchgear room during a postulated fire in that room, therefore affecting the reliability of the D emergency 4k switchgear gaseous suppression system to perform its safety function. The inspectors determined that this finding is of very low safety significance (Green) because it is a deficiency that affected the design or qualification of a mitigating structure, system, or component (SSC), where the SSC maintained its operability or functionality. This finding has a cross-cutting aspect in the area of Problem Identification and Resolution, Evaluation, because Exelon did not thoroughly evaluate issues to ensure that resolutions address the causes and extent of conditions commensurate with their safety significance. Specifically,
Exelon staff did not thoroughly evaluate the issue associated with the degraded floor gasket for fire and flood functionality. [P.2] (Section 1R06)
: '''Green.'''
: '''Green.'''
A self-revealing   determined the finding to be of very low safety significance (Green) knowledgeable, technically competent workforce 6
A self-revealing finding was identified associated with inadequate licensed operator performance during licensed operator requalification exams in accordance with TQ-AA-150,
Operator Training Program. Specifically, two of seven crews failed the simulator scenario portion of the requalification examinations. As an immediate corrective action, the crews that failed were restricted from licensed duties. Exelon entered this issue into the corrective action program, and facility training staff remediated the crews (the crews were retrained and successfully retested), and those crews were returned to licensed duties.
 
This finding is more than minor because it is associated with the human performance attribute of the Mitigating Systems cornerstone and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, two of seven crews failed to demonstrate a satisfactory understanding of the knowledge and abilities required to safely operate the facility under normal, abnormal, and emergency conditions. The inspectors determined the finding to be of very low safety significance (Green) because it is related to requalification exam results, did not result in a failure rate of greater than forty percent, and the two crews were remediated (i.e., the crews were retrained and successfully retested)prior to returning to shift. This finding has a cross-cutting aspect in the area of Human Performance, Training, because Exelon staff did not provide adequate operator requalification training to maintain a knowledgeable, technically competent workforce. [H.9]
(Section 1R11)


=REPORT DETAILS=
=REPORT DETAILS=
Summary of Plant Status Oyster Creek began the inspection period at 100 percent power. On May 7, 2015, an automatic reactor scram occurred due to a turbine trip caused by a failure of the main transformer digital protection relay system. After repairs to the digital protection relay system, operators commenced plant startup on May 12 and returned to full power operation on May
 
===Summary of Plant Status===
Oyster Creek began the inspection period at 100 percent power. On May 7, 2015, an automatic reactor scram occurred due to a turbine trip caused by a failure of the main transformer digital protection relay system. After repairs to the digital protection relay system, operators commenced plant startup on May 12 and returned to full power operation on May


==REACTOR SAFETY==
==REACTOR SAFETY==
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity  
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity  
{{a|1R01}}
 
{{a|1R01}}
 
==1R01 Adverse Weather Protection==
==1R01 Adverse Weather Protection==
{{IP sample|IP=IP 71111.01|count=2}}
{{IP sample|IP=IP 71111.01|count=2}}


===.1 Readiness for Seasonal Extreme Weather Conditions===
===.1 Readiness for Seasonal Extreme Weather Conditions===
====a. Inspection Scope====
The inspectors performed a review of Exelons readiness for the onset of seasonal high temperatures. The review focused on the emergency service water and the emergency diesel generators. The inspectors reviewed the Updated Final Safety Analysis Report (UFSAR), technical specifications, control room logs, and the corrective action program to determine what temperatures or other seasonal weather could challenge these systems, and to ensure Exelon personnel had adequately prepared for these challenges.


====a. Inspection Scope====
The inspectors reviewed station procedures, including Exelons seasonal weather preparation procedure and applicable operating procedures. The inspectors performed walkdowns of the selected systems to ensure station personnel identified issues that could challenge the operability of the systems during hot weather conditions.
The inspectors performed a review of  readiness for the onset of seasonal high temperatures. The review focused on the emergency service water and the emergency diesel generators. The inspectors reviewed the Updated Final Safety Analysis Report (UFSAR), technical specifications, control room logs, and the corrective action program to determine what temperatures or other seasonal weather could challenge these systems, and to ensure Exelon personnel had adequately prepared for these challenges. The inspectors reviewed station procedures, including seasonal weather preparation procedure and applicable operating procedures. The inspectors performed walkdowns of the selected systems to ensure station personnel identified issues that could challenge the operability of the systems during hot weather conditions. Documents reviewed for each section of this inspection report are listed in the Attachment.
 
Documents reviewed for each section of this inspection report are listed in the  
.


====b. Findings====
====b. Findings====
Line 64: Line 147:


===.2 Summer Readiness of Offsite and Alternate Alternating Current (AC) Power Systems===
===.2 Summer Readiness of Offsite and Alternate Alternating Current (AC) Power Systems===
====a. Inspection Scope====
====a. Inspection Scope====
The inspectors performed a review of plant features and procedures for the operation and continued availability of the offsite and alternate AC power system to evaluate readiness of the systems prior to seasonal high grid loading. The inspectors reviewed procedures affecting these areas and the communications protocols between the transmission system operator and Exelon. This review focused on changes to the established program and material condition of the offsite and alternate AC power equipment. The inspectors assessed whether Exelon established and implemented appropriate procedures and protocols to monitor and maintain availability and reliability of both the offsite AC power system and the onsite alternate AC power system. The inspectors evaluated the material condition of the associated equipment by interviewing the responsible system manager, reviewing condition reports and open work orders, and walking down portions of the offsite and AC power.
The inspectors performed a review of plant features and procedures for the operation and continued availability of the offsite and alternate AC power system to evaluate readiness of the systems prior to seasonal high grid loading. The inspectors reviewed Exelons procedures affecting these areas and the communications protocols between the transmission system operator and Exelon. This review focused on changes to the established program and material condition of the offsite and alternate AC power equipment. The inspectors assessed whether Exelon established and implemented appropriate procedures and protocols to monitor and maintain availability and reliability of both the offsite AC power system and the onsite alternate AC power system. The inspectors evaluated the material condition of the associated equipment by interviewing the responsible system manager, reviewing condition reports and open work orders, and walking down portions of the offsite and AC power.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R04}}
{{a|1R04}}
 
==1R04 Equipment Alignment==
==1R04 Equipment Alignment


==
===.1 Partial System Walkdowns===
===.1 Partial System Walkdowns===
{{IP sample|IP=IP 71111.04Q|count=5}}
{{IP sample|IP=IP 71111.04Q|count=5}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors performed partial walkdowns of the following systems:   Standby liquid control system on April 2, 2015 A,B,pump out of service on April 21, 2015 Turbine building closed cooling water system on April 28, 2015   forced outage (1F37) on May 12, 2015 No. 1 emergency diesel generator while No. 2 emergency diesel generator out of service on May 18, 2015 The inspectors selected these systems based on their risk-significance relative to the reactor safety cornerstones at the time they were inspected. The inspectors reviewed applicable operating procedures, system diagrams, the UFSAR, technical specifications, work orders, condition reports, and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have impacted the system performance of its intended safety functions. The inspectors also performed field walkdowns of accessible portions of the systems to verify system components and support equipment were aligned correctly and were operable. The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no deficiencies. The inspectors also reviewed whether Exelon staff had properly identified equipment issues and entered them into the corrective action program for resolution with the appropriate significance characterization.
The inspectors performed partial walkdowns of the following systems:  
 
Standby liquid control system on April 2, 2015  
 
A, B, and C emergency service water pumps while D emergency service water pump out of service on April 21, 2015  
 
Turbine building closed cooling water system on April 28, 2015  
 
A and B isolation condensers prior to startup from the forced outage (1F37) on May 12, 2015  
 
No. 1 emergency diesel generator while No. 2 emergency diesel generator out of service on May 18, 2015  
 
The inspectors selected these systems based on their risk-significance relative to the reactor safety cornerstones at the time they were inspected. The inspectors reviewed applicable operating procedures, system diagrams, the UFSAR, technical specifications, work orders, condition reports, and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have impacted the systems performance of its intended safety functions. The inspectors also performed field walkdowns of accessible portions of the systems to verify system components and support equipment were aligned correctly and were operable. The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no deficiencies. The inspectors also reviewed whether Exelon staff had properly identified equipment issues and entered them into the corrective action program for resolution with the appropriate significance characterization.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R05}}
{{a|1R05}}
 
==1R05 Fire Protection==
==1R05 Fire Protection


==
===.1 Resident Inspector Quarterly Walkdowns===
===.1 Resident Inspector Quarterly Walkdowns===
{{IP sample|IP=IP 71111.05Q|count=6}}
{{IP sample|IP=IP 71111.05Q|count=6}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors conducted tours of the areas listed below to assess the material condition and operational status of fire protection features. The inspectors verified that Exelon personnel controlled combustible materials and ignition sources in accordance with administrative procedures. The inspectors verified that fire protection and suppression equipment was available for use as specified in the area pre-fire plan, and passive fire barriers were maintained in good material condition. The inspectors also verified that station personnel implemented compensatory measures for out of service, degraded, or inoperable fire protection equipment, as applicable, in accordance with procedures.
The inspectors conducted tours of the areas listed below to assess the material condition and operational status of fire protection features. The inspectors verified that Exelon personnel controlled combustible materials and ignition sources in accordance with administrative procedures. The inspectors verified that fire protection and suppression equipment was available for use as specified in the area pre-fire plan, and passive fire barriers were maintained in good material condition. The inspectors also verified that station personnel implemented compensatory measures for out of service, degraded, or inoperable fire protection equipment, as applicable, in accordance with procedures.
 
Lower cable spreading room on April 8, 2015
 
Turbine building basement south on April 8, 2015
 
Feed pump room on April 8, 2015
 
Emergency diesel generator room No. 2 on April 15, 2015


Lower cable spreading room on April 8, 2015  Turbine building basement south on April 8, 2015  Feed pump room on April 8, 2015  Emergency diesel generator room No. 2 on April 15, 2015  Reactor building southeast corner room on April 15, 2015 Reactor building equipment drain tank room on May 19, 2015
Reactor building southeast corner room on April 15, 2015  
 
Reactor building equipment drain tank room on May 19, 2015


====b. Findings====
====b. Findings====
No findings were identified.  
No findings were identified.
{{a|1R06}}
 
{{a|1R06}}
 
==1R06 Flood Protection Measures==
==1R06 Flood Protection Measures==
{{IP sample|IP=IP 71111.06|count=3}}
{{IP sample|IP=IP 71111.06|count=3}}


===.1 Internal Flooding Review===
===.1 Internal Flooding Review===
====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the UFSAR, the site flooding analysis, and plant procedures to assess susceptibilities involving internal flooding. The inspectors also reviewed the corrective action program to determine if Exelon identified and corrected flooding problems and whether operator actions for coping with flooding were adequate. The inspectors focused on the reactor building southeast corner room area and turbine building switchgear area to verify the adequacy of equipment seals located below the flood line, floor and water penetration seals, watertight door seals, common drain lines and sumps, sump pumps, level alarms, control circuits, and temporary or removable flood barriers.
The inspectors reviewed the UFSAR, the site flooding analysis, and plant procedures to assess susceptibilities involving internal flooding. The inspectors also reviewed the corrective action program to determine if Exelon identified and corrected flooding problems and whether operator actions for coping with flooding were adequate. The inspectors focused on the reactor building southeast corner room area and turbine building switchgear area to verify the adequacy of equipment seals located below the flood line, floor and water penetration seals, watertight door seals, common drain lines and sumps, sump pumps, level alarms, control circuits, and temporary or removable flood barriers.


====b. Findings====
====b. Findings====
=====Introduction.=====
=====Introduction.=====
The inspectors identified a Green finding associated with Exelon procedure, OP-AA-108-115, Operability Determinations because Exelon did not adequately assess a degraded floor gasket for the switchgear roll-up door. Specifically, Exelon did not adequately assess the flood and fire functionality of the degraded gasket, which is credited to provide protection to the safety-related emergency 4kV switchgear during a postulated internal flood event and to contain the CO2 gaseous suppression system during a postulated fire within the room.
The inspectors identified a Green finding associated with Exelon procedure, OP-AA-108-115, Operability Determinations, because Exelon did not adequately assess a degraded floor gasket for the D emergency 4kV switchgear roll-up door. Specifically, Exelon did not adequately assess the flood and fire functionality of the degraded gasket, which is credited to provide protection to the safety-related D emergency 4kV switchgear during a postulated internal flood event and to contain the CO2 gaseous suppression system during a postulated fire within the D switchgear room.


=====Description.=====
=====Description.=====
During a system walk down on May 29, 2015, NRC inspectors identified a degraded floor gasket for the V switchgear roll-up door and informed Operations. Operations wrote issue report 2507389 to evaluate the degraded floor gasket flood functionality. The inspectors noted that the degraded floor gasket could postulated internal flood event due to a fire water pipe rupture. Specifically, OC-PSA-12, Internal Flood Evaluation Summary Notebook, states, The rollup doors have   The inspectors additionally identified that Operations did not consider the impact on the CO2 system and, as a result, did not establish a continuous fire watch with backup fire Exelon procedure 101.2, states, (penetration seals, dampers, doors, breaches in walls/floors/ceilings) could render a gaseous fire suppression system inoperable. In this event, the actions for an inoperable CO2 system and the actions for an inoperable fire rated assembly must be completed. With the CO2 system inoperable, within one hour, establish a continuous fire watch with   The inspectors noted that Exelon personnel originally identified the degraded floor gasket in December 2014 and documented this issue in issue report 2423574. The inspector reviewed the issue report and noted that Operations did not adequately evaluate the degraded barrier for flooding and fire functionality. The issue report stated that tegrity or ability to act as a fire door. Also, the issue report did not address the degraded The inspectors also reviewed issue report 2423574 to ascertain the corrective actions for the degraded floor gasket. The actions specified Exelon personnel to complete repairs to the floor gasket in work order R2249794. The actions in this work order were stated as complete, although the inspectors identified on May 29, 2015, the degraded floor gasket was not repaired.
During a system walk down on May 29, 2015, NRC inspectors identified a degraded floor gasket for the D emergency 4kV switchgear roll-up door and informed Operations. Operations wrote issue report 2507389 to evaluate the degraded floor gasket flood functionality. The inspectors noted that the degraded floor gasket could result in increased water level in the D emergency 4kV switchgear room during a postulated internal flood event due to a fire water pipe rupture. Specifically, OC-PSA-12, Internal Flood Evaluation Summary Notebook, states, in part, The rollup doors have gaskets along the bottom edge that are assumed to preclude water propagation.
 
The inspectors additionally identified that Operations did not consider the impact on the CO2 system and, as a result, did not establish a continuous fire watch with backup fire suppression equipment as stated in Exelon procedure 101.2, Oyster Creek Site Fire Protection Program. Exelon procedure 101.2, states, in part, an inoperable fire barrier (penetration seals, dampers, doors, breaches in walls/floors/ceilings) could render a gaseous fire suppression system inoperable. In this event, the actions for an inoperable CO2 system and the actions for an inoperable fire rated assembly must be completed.
 
With the CO2 system inoperable, within one hour, establish a continuous fire watch with backup fire suppression equipment.
 
The inspectors noted that Exelon personnel originally identified the degraded floor gasket in December 2014 and documented this issue in issue report 2423574. The inspector reviewed the issue report and noted that Operations did not adequately evaluate the degraded barrier for flooding and fire functionality. The issue report stated that the gasket did not affect the doors integrity or ability to act as a fire door. Also, the issue report did not address the degraded gaskets affect during internal flooding events.
 
The inspectors also reviewed issue report 2423574 to ascertain the corrective actions for the degraded floor gasket. The actions specified Exelon personnel to complete repairs to the floor gasket in work order R2249794. The actions in this work order were stated as complete, although the inspectors identified on May 29, 2015, the degraded floor gasket was not repaired.


The inspectors concluded that the degraded floor gasket was not properly assessed for fire or flooding functionality when Operations first identified the issue in December 2014 (issue report 2423574) and for fire functionality when the inspectors bought this issue to The inspectors determined that this is contrary to the requirements of OP-AA-108-115, Operability Determinations. This procedure the Technical Specifications, or they may be related to support functions for system, structure and component (SSC) in the TS. Examples of structural degradation are degradation of   OP-AA-108-115-1002, Supplemental Consideration for On-Shift Immediate Operability Determinations, states, in part, the ability of a SSC to meet regulatory requirements, codes, industry standards, (e.g., Fire Protection analysis, Appendix R, Safe Shutdown capability) or non-conformances affecting internal flooding concerns are thoroughly assessed.
The inspectors concluded that the degraded floor gasket was not properly assessed for fire or flooding functionality when Operations first identified the issue in December 2014 (issue report 2423574) and for fire functionality when the inspectors bought this issue to Operations attention on May 29, 2015. The inspectors determined that this is contrary to the requirements of OP-AA-108-115, Operability Determinations. This procedure states in part, Structures may be required to be operable by the Technical Specifications, or they may be related to support functions for system, structure and component (SSC) in the TS. Examples of structural degradation are degradation of door and penetration sealing. If a structure is degraded, the structures capability of performing its specified function should be assessed. Also, Exelon procedure OP-AA-108-115-1002, Supplemental Consideration for On-Shift Immediate Operability Determinations, states, in part, the ability of a SSC to meet regulatory requirements, codes, industry standards, (e.g., Fire Protection analysis, Appendix R, Safe Shutdown capability) or non-conformances affecting internal flooding concerns are thoroughly assessed.


Immediate corrective actions, following identification by the inspectors, included placing a sandbag in the area of the degraded gasket. As additional corrective actions, Exelon conducted a detailed analysis of the degraded gasket to determine if the flooding and fire functions were affected. switchgear room due to the degraded gasket was below the level that would impact the Exelon determined that the CO2 system could compensate for leakage through the degraded gasket and would still be capable of extinguishing a postulated fire within the Also, corrective actions included reinforcing the operability determination procedure, enhancing operator training in fire and flood functionality of gaskets, and repairing the gasket.
Immediate corrective actions, following identification by the inspectors, included placing a sandbag in the area of the degraded gasket. As additional corrective actions, Exelon conducted a detailed analysis of the degraded gasket to determine if the flooding and fire functions were affected. Exelon determined that the increase of water level in the D switchgear room due to the degraded gasket was below the level that would impact the D switchgear during the postulated fire water pipe break. Exelon determined that the CO2 system could compensate for leakage through the degraded gasket and would still be capable of extinguishing a postulated fire within the D switchgear room. Also, corrective actions included reinforcing the operability determination procedure, enhancing operator training in fire and flood functionality of gaskets, and repairing the gasket.


=====Analysis.=====
=====Analysis.=====
The inspectors determined that inadequate assessment for fire or flooding functionality of the -up door degraded floor gasket, in accordance with OP-AA-108-115, is and correct. The finding is more than minor because it is associated with the protection against external factors attribute of the Mitigating Systems cornerstone and affected the cornerstone objective to ensure the reliability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the degraded floor gasket could have resulted in increased water level in the postulated internal flood due to a fire water pipe rupture, therefore affecting the reliability of the In addition, the degraded floor gasket could have resulted in CO2 switchgear room during a postulated fire in that room, therefore affecting the reliability of function.
The inspectors determined that inadequate assessment for fire or flooding functionality of the D switchgear roll-up door degraded floor gasket, in accordance with OP-AA-108-115, is a performance deficiency that was within Exelons ability to foresee and correct. The finding is more than minor because it is associated with the protection against external factors attribute of the Mitigating Systems cornerstone and affected the cornerstone objective to ensure the reliability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the degraded floor gasket could have resulted in increased water level in the D emergency 4k switchgear room during a postulated internal flood due to a fire water pipe rupture, therefore affecting the reliability of the D emergency 4k switchgear to perform its safety function. In addition, the degraded floor gasket could have resulted in CO2 leakage out of the D emergency 4k switchgear room during a postulated fire in that room, therefore affecting the reliability of the D emergency 4k switchgear gaseous suppression system to perform its safety function.


The inspectors evaluated the finding using and IMC 0609, Appendix A, Einspectors determined that this finding is a deficiency that affected the design or qualification of a mitigating SSC, where the SSC maintained its operability or functionality. Therefore, inspectors determined the finding to be of very low safety significance (Green).
The inspectors evaluated the finding using 0609.04, Initial Characterization of Findings, and IMC 0609, Appendix A, Exhibit 2, Mitigating System Screening Questions. The inspectors determined that this finding is a deficiency that affected the design or qualification of a mitigating SSC, where the SSC maintained its operability or functionality. Therefore, inspectors determined the finding to be of very low safety significance (Green).


This finding has a cross-cutting aspect in the area of Problem Identification and Resolution, Evaluation, because Exelon did not thoroughly evaluate issues to ensure that resolutions address the causes and extent of conditions commensurate with their safety significance. Specifically, Exelon staff did not thoroughly evaluate the issue associated with the degraded floor gasket for fire and flood functionality. [P.2]  
This finding has a cross-cutting aspect in the area of Problem Identification and Resolution, Evaluation, because Exelon did not thoroughly evaluate issues to ensure that resolutions address the causes and extent of conditions commensurate with their safety significance. Specifically, Exelon staff did not thoroughly evaluate the issue associated with the degraded floor gasket for fire and flood functionality. [P.2]  


=====Enforcement.=====
=====Enforcement.=====
This finding does not involve enforcement action because no violation of regulatory requirements was identified. Exelon entered this issue into their corrective action program as issue report 2507389. Because this issue did not involve a violation and has very low safety significance, it is identified as a finding. (FIN 05000219/2015002-01, Inadequate Assessment of 4kV Emergency Switchgear Roll-Up Door Degraded Floor Gasket).
This finding does not involve enforcement action because no violation of regulatory requirements was identified. Exelon entered this issue into their corrective action program as issue report 2507389. Because this issue did not involve a violation and has very low safety significance, it is identified as a finding. (FIN  
 
===05000219/2015002-01, Inadequate Assessment of 4kV Emergency Switchgear Roll-Up Door Degraded Floor Gasket).


===.2 Annual Review of Cables Located in Underground Bunkers/Manholes===
===.2 Annual Review of Cables Located in Underground Bunkers/Manholes===
====a. Inspection Scope====
====a. Inspection Scope====
The inspectors conducted an inspection of underground bunkers/manholes subject to flooding that contain cables whose failure could disable risk-significant equipment.
The inspectors conducted an inspection of underground bunkers/manholes subject to flooding that contain cables whose failure could disable risk-significant equipment.


The inspectors performed walkdowns of risk-significant areas, including the SBO3 (MH-743-3), containing 13.8kV cables from the combusting turbine, and the intake area manhole (MH-731-1), containing 4160V cables from the emergency service water pumps, to verify that the cables were not submerged in water, that cables and/or splices appeared intact, and to observe the condition of cable support structures. When applicable, the inspectors verified proper sump pump operation and verified level alarm circuits were set in accordance with station procedures and calculations to ensure that the cables will not be submerged. The inspectors also ensured that drainage was provided and functioning properly in areas where dewatering devices were not installed.
The inspectors performed walkdowns of risk-significant areas, including the SBO3 (MH-743-3), containing 13.8kV cables from the combusting turbine, and the intake area manhole (MH-731-1), containing 4160V cables from the emergency service water pumps, to verify that the cables were not submerged in water, that cables and/or splices appeared intact, and to observe the condition of cable support structures. When applicable, the inspectors verified proper sump pump operation and verified level alarm circuits were set in accordance with station procedures and calculations to ensure that the cables will not be submerged. The inspectors also ensured that drainage was provided and functioning properly in areas where dewatering devices were not installed.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R07}}
{{a|1R07}}
 
==1R07 Heat Sink Performance (711111.07A==
==1R07 Heat Sink Performance (711111.07A - 1 sample)
1 sample)


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the 1-1 reactor building closed cooling water heat exchanger to determine its readiness and availability to perform its safety functions. The inspectors reviewed the design basis for the component and verified commitments to NRC Generic Letter 89-13. The inspectors reviewed the cleaning and inspection of the heat exchanger, discussed the results of the most recent inspection with engineering staff, and reviewed pictures of the as-found and as-left conditions. The inspectors verified that Exelon initiated appropriate corrective actions for identified deficiencies. The inspectors also verified that the number of tubes plugged within the heat exchanger did not exceed the maximum amount allowed.
==
The inspectors reviewed the 1-1 reactor building closed cooling water heat exchanger to determine its readiness and availability to perform its safety functions. The inspectors reviewed the design basis for the component and verified Exelons commitments to NRC Generic Letter 89-13. The inspectors reviewed the cleaning and inspection of the heat exchanger, discussed the results of the most recent inspection with engineering staff, and reviewed pictures of the as-found and as-left conditions. The inspectors verified that Exelon initiated appropriate corrective actions for identified deficiencies. The inspectors also verified that the number of tubes plugged within the heat exchanger did not exceed the maximum amount allowed.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R11}}
{{a|1R11}}
 
==1R11 Licensed Operator Requalification Program==
==1R11 Licensed Operator Requalification Program


==
===.1 Quarterly Review of Licensed Operator Requalification Testing and Training===
===.1 Quarterly Review of Licensed Operator Requalification Testing and Training===
{{IP sample|IP=IP 71111.11Q|count=1}}
(71111.11Q - 1 sample)


====a. Inspection Scope====
====a. Inspection Scope====
Line 156: Line 272:


===.2 Quarterly Review of Licensed Operator Performance in the Main Control Room===
===.2 Quarterly Review of Licensed Operator Performance in the Main Control Room===
{{IP sample|IP=IP 71111.11Q|count=1}}
(71111.11Q - 1 sample)


====a. Inspection Scope====
====a. Inspection Scope====
Line 168: Line 284:


====a. Inspection Scope====
====a. Inspection Scope====
The following inspection activities were performed using The inspection assessed whether pass rates were consistent with the Human Performance Significance Determination Process (SDP). Examination Results On July 1, 2015, the results of the comprehensive written and annual operating tests were reviewed to determine if pass/fail rates were consistent with the guidance of NUREG-1021, Rereview determined that the individual operator failure rate was less than 20 percent, however, the crew failure rate exceeded 20 percent.
The following inspection activities were performed using NUREG-1021, "Operator Licensing Examination Standards for Power Reactors," Revision 9, Supplement 1, and Inspection Procedure Attachment 71111.11, Licensed Operator Requalification Program. The inspection assessed whether pass rates were consistent with the guidance of NRC Manual Chapter 0609, Appendix I, and Operator Requalification Human Performance Significance Determination Process (SDP).
 
Examination Results  
 
On July 1, 2015, the results of the comprehensive written and annual operating tests were reviewed to determine if pass/fail rates were consistent with the guidance of NUREG-1021, Revision 9, Supplement 1 and NRC IMC 0609, Appendix I, Operator Requalification Human Performance Significance Determination Process (SDP). The review determined that the individual operator failure rate was less than 20 percent, however, the crew failure rate exceeded 20 percent.


====b. Findings====
====b. Findings====
=====Introduction:=====
=====Introduction:=====
A self-revealing Green finding was identified associated with inadequate licensed operator performance during licensed operator requalification exams in accordance with TQ-AA-.crews failed the simulator scenario portion of the requalification examinations.
A self-revealing Green finding was identified associated with inadequate licensed operator performance during licensed operator requalification exams in accordance with TQ-AA-150, Operator Training Program. Specifically, two of seven crews failed the simulator scenario portion of the requalification examinations.


=====Description:=====
=====Description:=====
During the administered requalification examinations to licensed operators. Exelon staff evaluated crew performance during dynamic simulator scenarios and individual operator performance during job performance measures and on the written examination. Exelon evaluation of the requalification examination showed that two of seven crews (which represents a failure rate of 28.6 percent) failed the simulator scenario portion of the examination. This failure rate exceeded the threshold failure rate of 20 percent as specified in TQ-AA-150, . part, that simulator crew failure rate greater than 20 percent but less than 40 percent constitutes as a Green finding. Exelon initiated issue report 2513013 to address the high failure rate on the annual requalification examinations, restricted the failed crews from licensed duties, conducted crew and individual operator remediation, and began conducting a root cause evaluation to develop long-term corrective actions.  
During the week of June 8, 2015, Exelons training staff administered requalification examinations to licensed operators. Exelon staff evaluated crew performance during dynamic simulator scenarios and individual operator performance during job performance measures and on the written examination. Exelon evaluation of the requalification examination showed that two of seven crews (which represents a failure rate of 28.6 percent) failed the simulator scenario portion of the examination. This failure rate exceeded the threshold failure rate of 20 percent as specified in TQ-AA-150, Operator Training Program. Specifically, Attachment F25, LORT Annual Exam Status Report states, in part, that simulator crew failure rate greater than 20 percent but less than 40 percent constitutes as a Green finding.
 
Exelon initiated issue report 2513013 to address the high failure rate on the annual requalification examinations, restricted the failed crews from licensed duties, conducted crew and individual operator remediation, and began conducting a root cause evaluation to develop long-term corrective actions.


=====Analysis:=====
=====Analysis:=====
The inspectors determined that the crew failure rate of greater than 20 percent, as specified in TQ-AA-150, is a performance deficiency that was reasonably This finding is more than minor because it is associated with the Mitigating Systems cornerstone attribute of human performance and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, two of seven crews failed to demonstrate a satisfactory understanding of the knowledge and abilities required to safely operate the facility under normal, abnormal, and emergency conditions. Licensed operators are expected to operate the plant within acceptable standards of knowledge and abilities demonstrated through periodic testing. The inspectors evaluated this performance deficiency using Inspection Manual Chapter 0609.04, "Initial Characterization of Findings," Appendix I, "Licensed Operator Requalification Significance Determination Process." This finding is of very low safety significance (Green) because the finding is related to requalification exam results, did not result in a failure rate of greater than 40 percent, and the two crews were remediated (i.e., the licensed operators were retrained and successfully retested) prior to returning to shift.
The inspectors determined that the crew failure rate of greater than 20 percent, as specified in TQ-AA-150, is a performance deficiency that was reasonably within Exelons ability to foresee and correct. This finding is more than minor because it is associated with the Mitigating Systems cornerstone attribute of human performance and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, two of seven crews failed to demonstrate a satisfactory understanding of the knowledge and abilities required to safely operate the facility under normal, abnormal, and emergency conditions. Licensed operators are expected to operate the plant within acceptable standards of knowledge and abilities demonstrated through periodic testing. The inspectors evaluated this performance deficiency using Inspection Manual Chapter 0609.04, "Initial Characterization of Findings," Appendix I, "Licensed Operator Requalification Significance Determination Process." This finding is of very low safety significance (Green) because the finding is related to requalification exam results, did not result in a failure rate of greater than 40 percent, and the two crews were remediated (i.e., the licensed operators were retrained and successfully retested)prior to returning to shift.
 
This finding has a cross-cutting aspect in the area of Human Performance, Training, because Exelon did not initially provide adequate operator requalification training to maintain a knowledgeable, technically competent workforce. [H.9]


knowledgeable, technically competent workforce  and has very low safety significance (Green), it is identified as a finding. (FIN 05000219/2015002-02, Failure Rates Exceed Twenty Percent for Annual Requalification Exam).
=====Enforcement:=====
This finding does not involve enforcement action because no violation of regulatory requirements was identified. Exelon entered this issue into their corrective action program as issue report 2513013. Because this issue did not involve a violation and has very low safety significance (Green), it is identified as a finding.
 
(FIN 05000219/2015002-02, Failure Rates Exceed Twenty Percent for Annual Requalification Exam).


{{a|1R12}}
{{a|1R12}}
==1R12 Maintenance Effectiveness==
==1R12 Maintenance Effectiveness==
{{IP sample|IP=IP 71111.12|count=2}}
{{IP sample|IP=IP 71111.12|count=2}}
Line 190: Line 317:
The inspectors reviewed the samples listed below to assess the effectiveness of maintenance activities on SSC performance and reliability. The inspectors reviewed system health reports, corrective action program documents, maintenance work orders, and maintenance rule basis documents to ensure that Exelon was identifying and properly evaluating performance problems within the scope of the maintenance rule.
The inspectors reviewed the samples listed below to assess the effectiveness of maintenance activities on SSC performance and reliability. The inspectors reviewed system health reports, corrective action program documents, maintenance work orders, and maintenance rule basis documents to ensure that Exelon was identifying and properly evaluating performance problems within the scope of the maintenance rule.


For each sample selected, the inspectors verified that the SSC was properly scoped into the maintenance rule in accordance with 10 CFR 50.65 and verified that the (a)(2) performance criteria established by Exelon staff was reasonable. As applicable, for a SSC classified as (a)(1), the inspectors assessed the adequacy of goals and corrective actions to return the SSC to (a)(2). Additionally, the inspectors ensured that Exelon staff was identifying and addressing common cause failures that occurred within and across maintenance rule system boundaries.
For each sample selected, the inspectors verified that the SSC was properly scoped into the maintenance rule in accordance with 10 CFR 50.65 and verified that the (a)(2)performance criteria established by Exelon staff was reasonable. As applicable, for a SSC classified as (a)(1), the inspectors assessed the adequacy of goals and corrective actions to return the SSC to (a)(2). Additionally, the inspectors ensured that Exelon staff was identifying and addressing common cause failures that occurred within and across maintenance rule system boundaries.
 
Core spray system on June 2, 2015


Core spray system on June 2, 2015  Main transformers digital protection relay system on May 20, 2015
Main transformers digital protection relay system on May 20, 2015


====b. Findings====
====b. Findings====
No findings were identified.  
No findings were identified.
{{a|1R13}}
 
{{a|1R13}}
 
==1R13 Maintenance Risk Assessments and Emergent Work Control==
==1R13 Maintenance Risk Assessments and Emergent Work Control==
{{IP sample|IP=IP 71111.13|count=5}}
{{IP sample|IP=IP 71111.13|count=5}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed station evaluation and management of plant risk for the maintenance and emergent work activities listed below to verify that Exelon performed the appropriate risk assessments prior to removing equipment for work. The inspectors selected these activities based on potential risk significance relative to the reactor safety cornerstones. As applicable for each activity, the inspectors verified that Exelon personnel performed risk assessments as required by 10 CFR 50.65(a)(4) and that the assessments were accurate and complete. When Exelon performed emergent work, the inspectors verified that operations personnel promptly assessed and managed plant risk. The inspectors reviewed the scope of maintenance work and discussed the results owith the risk assessment. The inspectors also reviewed the technical specification requirements and inspected portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met.
The inspectors reviewed station evaluation and management of plant risk for the maintenance and emergent work activities listed below to verify that Exelon performed the appropriate risk assessments prior to removing equipment for work. The inspectors selected these activities based on potential risk significance relative to the reactor safety cornerstones. As applicable for each activity, the inspectors verified that Exelon personnel performed risk assessments as required by 10 CFR 50.65(a)(4) and that the assessments were accurate and complete. When Exelon performed emergent work, the inspectors verified that operations personnel promptly assessed and managed plant risk. The inspectors reviewed the scope of maintenance work and discussed the results of the assessment with Exelons risk analyst to verify plant conditions were consistent with the risk assessment. The inspectors also reviewed the technical specification requirements and inspected portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met.
 
A isolation condenser out of service for planned maintenance on April 1, 2015
 
B reactor building closed loop cooling water pump out for planned maintenance on April 21, 2015
 
1-2 service water pump out of service for planned maintenance on May 4, 2015
 
Forced outage yellow shutdown risk due to decay heat removal on May 8, 2015


A isolation condenser out of service for planned maintenance on April 1, 2015  on April 21, 2015  1-2 service water pump out of service for planned maintenance on May 4, 2015  Forced outage yellow shutdown risk due to decay heat removal on May 8, 2015  No. 2 emergency diesel generator out of service for planned maintenance on May 18, 2015
No. 2 emergency diesel generator out of service for planned maintenance on May 18, 2015


====b. Findings====
====b. Findings====
No findings were identified.  
No findings were identified.
{{a|1R15}}
 
{{a|1R15}}
 
==1R15 Operability Determinations and Functionality Assessments==
==1R15 Operability Determinations and Functionality Assessments==
{{IP sample|IP=IP 71111.15|count=6}}
{{IP sample|IP=IP 71111.15|count=6}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed operability determinations for the following degraded or non-conforming conditions:   Standby liquid control accumulator (Y-19-101) at 0 psig on April 1, 2015 Core spray booster pump (NZ03A) due to high differential pressure on June 2, 2015 Spent fuel pool boraflex fuel racks on June 3, 2015 Containment spray 51A breaker loose arc chutes on June 19, 2015 Emergency service water system I while spectacle flange in orifice position on June 22, 2015 Electromatic relief valve cutout switch part 21 on June 23, 2015 The inspectors selected these issues based on the risk significance of the associated components and systems. The inspectors evaluated the technical adequacy of the operability determinations to assess whether technical specification operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the technical specifications and UFSAR to evaluations to determine whether the components or systems were operable. The inspectors determined, where appropriate, compliance with bounding limitations associated with the evaluations. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled by Exelon.
The inspectors reviewed operability determinations for the following degraded or non-conforming conditions:  
 
Standby liquid control accumulator (Y-19-101) at 0 psig on April 1, 2015  
 
Core spray booster pump (NZ03A) due to high differential pressure on June 2, 2015  
 
Spent fuel pool boraflex fuel racks on June 3, 2015  
 
Containment spray 51A breaker loose arc chutes on June 19, 2015  
 
Emergency service water system I while spectacle flange in orifice position on June 22, 2015  
 
Electromatic relief valve cutout switch part 21 on June 23, 2015  
 
The inspectors selected these issues based on the risk significance of the associated components and systems. The inspectors evaluated the technical adequacy of the operability determinations to assess whether technical specification operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the technical specifications and UFSAR to Exelons evaluations to determine whether the components or systems were operable.
 
The inspectors determined, where appropriate, compliance with bounding limitations associated with the evaluations. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled by Exelon.


====b. Findings====
====b. Findings====
No findings were identified.  
No findings were identified.
{{a|1R18}}
 
{{a|1R18}}
 
==1R18 Plant Modifications==
==1R18 Plant Modifications==
{{IP sample|IP=IP 71111.18|count=3}}
{{IP sample|IP=IP 71111.18|count=3}}


===.1 Temporary Modifications===
===.1 Temporary Modifications===
====a. Inspection Scope====
The inspectors reviewed the temporary modifications listed below to determine whether the modifications affected the safety functions of systems that are important to safety.


====a. Inspection Scope====
The inspectors reviewed 10 CFR 50.59 documentation and post-modification testing results, and conducted field walkdowns of the modifications to verify that the temporary modifications did not degrade the design bases, licensing bases, and performance capability of the affected systems.
The inspectors reviewed the temporary modifications listed below to determine whether the modifications affected the safety functions of systems that are important to safety. The inspectors reviewed 10 CFR 50.59 documentation and post-modification testing results, and conducted field walkdowns of the modifications to verify that the temporary modifications did not degrade the design bases, licensing bases, and performance capability of the affected systems.


Temporary configuration change TCC-1504-532-RO-22 Emergency service water system I to service water cross connect by rotating a spectacle flange on May 29, 2015
Temporary configuration change TCC-1504-532-RO-22 - Emergency service water system I to service water cross connect by rotating a spectacle flange on May 29, 2015


====b. Findings====
====b. Findings====
Line 231: Line 391:


===.2 Permanent Modifications===
===.2 Permanent Modifications===
====a. Inspection Scope====
====a. Inspection Scope====
The inspectors evaluated a modification to the automatic scram contactors surveillance test frequency by surveillance test interval evaluation form OC-15- The inspectors also evaluated a modification to the main transformer digital protection relay system by engineering change request 15-The inspectors verified that the design bases, licensing bases, and performance capability of the affected systems were not degraded by the modification. In addition, the inspectors reviewed modification documents associated with the upgrade and design changes. The inspectors also reviewed revisions to the control room alarm response procedures and interviewed engineering and operations personnel to ensure the procedure could be reasonably performed.
The inspectors evaluated a modification to the automatic scram contactors surveillance test frequency by surveillance test interval evaluation form OC-15-01, Automatic SCRAM Contactor Surveillance Extension. The inspectors also evaluated a modification to the main transformer digital protection relay system by engineering change request 15-00197, ECR to Remove the Output Trip Functions from the Digital Protection Relay System. The inspectors verified that the design bases, licensing bases, and performance capability of the affected systems were not degraded by the modification. In addition, the inspectors reviewed modification documents associated with the upgrade and design changes. The inspectors also reviewed revisions to the control room alarm response procedures and interviewed engineering and operations personnel to ensure the procedure could be reasonably performed.


====b. Findings====
====b. Findings====
No findings were identified.  
No findings were identified.
{{a|1R19}}
 
{{a|1R19}}
 
==1R19 Post-Maintenance Testing==
==1R19 Post-Maintenance Testing==
{{IP sample|IP=IP 71111.19|count=4}}
{{IP sample|IP=IP 71111.19|count=4}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the post-maintenance tests for the maintenance activities listed below to verify that procedures and test activities adequately tested the safety functions that may have been affected by the maintenance activity, that the acceptance criteria in the procedure was consistent with the information in the applicable licensing basis and/or design basis documents, and that the test results were properly reviewed and accepted and problems were appropriately documented. The inspectors also walked down the affected job site, observed the pre-job brief and post-job critique where possible, confirmed work site cleanliness was maintained, and witnessed the test or reviewed test data to verify quality control hold point were performed and checked, and that results adequately demonstrated restoration of the affected safety functions.
The inspectors reviewed the post-maintenance tests for the maintenance activities listed below to verify that procedures and test activities adequately tested the safety functions that may have been affected by the maintenance activity, that the acceptance criteria in the procedure was consistent with the information in the applicable licensing basis and/or design basis documents, and that the test results were properly reviewed and accepted and problems were appropriately documented. The inspectors also walked down the affected job site, observed the pre-job brief and post-job critique where possible, confirmed work site cleanliness was maintained, and witnessed the test or reviewed test data to verify quality control hold point were performed and checked, and that results adequately demonstrated restoration of the affected safety functions.
 
Hydraulic control unit 46-39 following cooling water check valve (V-305-138)replacement on April 6, 2015


Hydraulic control unit 46-39 following cooling water check valve (V-305-138) replacement on April 6, 2015  following mp motor replacement on April 22, 2015 Main transformers after sudden pressure relay addition on May 18, 2015 Emergency diesel generator No. 2 following battery replacement on May 19, 2015
D emergency service water pump following D emergency service water pump motor replacement on April 22, 2015  
 
Main transformers after sudden pressure relay addition on May 18, 2015  
 
Emergency diesel generator No. 2 following battery replacement on May 19, 2015


====b. Findings====
====b. Findings====
No findings were identified.  
No findings were identified.
{{a|1R20}}
 
{{a|1R20}}
 
==1R20 Refueling and Other Outage Activities==
==1R20 Refueling and Other Outage Activities==
{{IP sample|IP=IP 71111.20|count=1}}
{{IP sample|IP=IP 71111.20|count=1}}


====a. Inspection Scope====
====a. Inspection Scope====
Creek forced outage (1F37), which was conducted May 7 through May 14, 2015. The schedules to verify that risk, industry experience, previous site-specific problems, and defense-in-depth were considered. During the outage, the inspectors observed portions of the shutdown and cooldown processes and monitored controls associated with the following outage activities:   Configuration management, including maintenance of defense-in-depth, commensurate with the outage plan for the key safety functions and compliance with the applicable technical specifications when taking equipment out of service Implementation of clearance activities and confirmation that tags were properly hung and that equipment was appropriately configured to safely support the associated work or testing Installation and configuration of reactor coolant pressure, level, and temperature instruments to provide accurate indication and instrument error accounting   Status and configuration of electrical systems and switchyard activities to ensure that technical specifications were met Monitoring of decay heat removal operations Impact of outage work on the ability of the operators to operate the spent fuel pool cooling system Reactor water inventory controls, including flow paths, configurations, alternative means for inventory additions, and controls to prevent inventory loss Activities that could affect reactivity   Maintenance of secondary containment as required by technical specifications Fatigue management Identification and resolution of problems related to refueling outage activities
The inspectors reviewed the stations work schedule and outage risk plan for Oyster Creek forced outage (1F37), which was conducted May 7 through May 14, 2015. The inspectors reviewed Exelons development and implementation of outage plans and schedules to verify that risk, industry experience, previous site-specific problems, and defense-in-depth were considered. During the outage, the inspectors observed portions of the shutdown and cooldown processes and monitored controls associated with the following outage activities:  
 
Configuration management, including maintenance of defense-in-depth, commensurate with the outage plan for the key safety functions and compliance with the applicable technical specifications when taking equipment out of service  
 
Implementation of clearance activities and confirmation that tags were properly hung and that equipment was appropriately configured to safely support the associated work or testing  
 
Installation and configuration of reactor coolant pressure, level, and temperature instruments to provide accurate indication and instrument error accounting  
 
Status and configuration of electrical systems and switchyard activities to ensure that technical specifications were met  
 
Monitoring of decay heat removal operations  
 
Impact of outage work on the ability of the operators to operate the spent fuel pool cooling system  
 
Reactor water inventory controls, including flow paths, configurations, alternative means for inventory additions, and controls to prevent inventory loss  
 
Activities that could affect reactivity  
 
Maintenance of secondary containment as required by technical specifications  
 
Fatigue management  
 
Identification and resolution of problems related to refueling outage activities


====b. Findings====
====b. Findings====
No findings were identified.  
No findings were identified.
{{a|1R22}}
 
{{a|1R22}}
 
==1R22 Surveillance Testing==
==1R22 Surveillance Testing==
{{IP sample|IP=IP 71111.22|count=5}}
{{IP sample|IP=IP 71111.22|count=5}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors observed performance of surveillance tests and/or reviewed test data of selected risk-significant SSCs to assess whether test results satisfied technical specifications, the UFSAR, and Exelon procedure requirements. The inspectors verified that test acceptance criteria were clear, tests demonstrated operational readiness and were consistent with design documentation, test instrumentation had current calibrations and the range and accuracy for the application, tests were performed as written, and applicable test prerequisites were satisfied. Upon test completion, the inspectors considered whether the test results supported that equipment was capable of performing the required safety functions. The inspectors reviewed the following surveillance tests:   A isolation condenser test and calibration on April 1, 2015 B isolation condenser valve operability and in-service test (IST) on April 7, 2015 (IST) Unidentified reactor coolant system (RCS) leak rate verification on May 7, 2015 (RCS) tion on May 8, 2015 Core spray system II valve operability and IST on May 19, 2015
The inspectors observed performance of surveillance tests and/or reviewed test data of selected risk-significant SSCs to assess whether test results satisfied technical specifications, the UFSAR, and Exelon procedure requirements. The inspectors verified that test acceptance criteria were clear, tests demonstrated operational readiness and were consistent with design documentation, test instrumentation had current calibrations and the range and accuracy for the application, tests were performed as written, and applicable test prerequisites were satisfied. Upon test completion, the inspectors considered whether the test results supported that equipment was capable of performing the required safety functions. The inspectors reviewed the following surveillance tests:  
 
A isolation condenser test and calibration on April 1, 2015  
 
B isolation condenser valve operability and in-service test (IST) on April 7, 2015 (IST)  
 
Unidentified reactor coolant system (RCS) leak rate verification on May 7, 2015 (RCS)  
 
B isolation condenser sensor test and calibration on May 8, 2015  
 
Core spray system II valve operability and IST on May 19, 2015


====b. Findings====
====b. Findings====
No findings were identified. Cornerstone: Emergency Preparedness  
No findings were identified.  
{{a|1EP6}}
 
===Cornerstone: Emergency Preparedness===
{{a|1EP6}}
 
==1EP6 Drill Evaluation==
==1EP6 Drill Evaluation==
{{IP sample|IP=IP 71114.06|count=1}}
{{IP sample|IP=IP 71114.06|count=1}}


===.1 Training Observations===
===.1 Training Observations===
====a. Inspection Scope====
====a. Inspection Scope====
The inspectors observed a simulator training evolution for licensed operators on April 14, 2015, which required emergency plan implementation by an operations crew. Exelon planned for this evolution to be evaluated and included in performance indicator data regarding drill and exercise performance. The inspectors observed event classification and notification activities performed by the crew. The inspectors also attended the post-as to note any Exelon evaluators noted the same issues and entered them into the corrective action program.
The inspectors observed a simulator training evolution for licensed operators on April 14, 2015, which required emergency plan implementation by an operations crew. Exelon planned for this evolution to be evaluated and included in performance indicator data regarding drill and exercise performance. The inspectors observed event classification and notification activities performed by the crew. The inspectors also attended the post-evolution critique for the scenario. The focus of the inspectors activities was to note any weaknesses and deficiencies in the crews performance and ensure that Exelon evaluators noted the same issues and entered them into the corrective action program.


====b. Findings====
====b. Findings====
Line 279: Line 484:


==RADIATION SAFETY==
==RADIATION SAFETY==
===Cornerstone: Occupational and Public Radiation Safety===
{{a|2RS5}}


===Cornerstone: Occupational and Public Radiation Safety
{{a|2RS5}}
==2RS5 Radiation Monitoring Instrumentation==
==2RS5 Radiation Monitoring Instrumentation==
{{IP sample|IP=IP 71124.05|count=1}}
{{IP sample|IP=IP 71124.05|count=1}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed performance in assuring the accuracy and operability of radiation monitoring instruments used to protect occupational workers and for effluent monitoring and analysis. The inspectors used the requirements in 10 CFR 20; 10 CFR 50, Appendix I; technical specifications; Offsite Dose Calculation Manual (ODCM);===
The inspectors reviewed performance in assuring the accuracy and operability of radiation monitoring instruments used to protect occupational workers and for effluent monitoring and analysis. The inspectors used the requirements in 10 CFR 20; 10 CFR 50, Appendix I; technical specifications; Offsite Dose Calculation Manual (ODCM);regulatory guides; applicable industry standards; and procedures required by technical specifications as criteria for determining compliance.


regulatory guides; applicable industry standards; and procedures required by technical specifications as criteria for determining compliance. Calibration and Testing Program For the gaseous and liquid effluent radiation monitor instrumentation, the inspectors reviewed the current detector and electronic channel calibrations, functional testing results and alarm set-points.
Calibration and Testing Program  
 
For the gaseous and liquid effluent radiation monitor instrumentation, the inspectors reviewed the current detector and electronic channel calibrations, functional testing results and alarm set-points.


====b. Findings====
====b. Findings====
{{a|2RS6}}
No findings were identified.
 
{{a|2RS6}}
 
==2RS6 Radioactive Gaseous and Liquid Effluent Treatment==
==2RS6 Radioactive Gaseous and Liquid Effluent Treatment==
{{IP sample|IP=IP 71124.06|count=1}}
{{IP sample|IP=IP 71124.06|count=1}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the treatment, monitoring, and control of radioactive gaseous and liquid effluents. The inspectors used the requirements in 10 CFR 20; 10 CFR 50, Appendix I; technical specifications; ODCM; applicable industry standards; and procedures required by technical specifications as criteria for determining compliance.
The inspectors reviewed the treatment, monitoring, and control of radioactive gaseous and liquid effluents. The inspectors used the requirements in 10 CFR 20; 10 CFR 50, Appendix I; technical specifications; ODCM; applicable industry standards; and procedures required by technical specifications as criteria for determining compliance.


=====Inspection Planning=====
=====Inspection Planning=====
The inspectors conducted in-office review of the Oyster Creek 2013 and 2014 annual radioactive effluent release reports, radioactive effluent program documents, UFSAR, ODCM, and applicable event reports. Walk-downs and Observations The inspectors walked down the gaseous and liquid radioactive effluent monitoring systems to assess the material condition and verify proper alignment according to plant design. The inspectors also observed potential unmonitored release points and reviewed radiation monitoring system surveillance records and the routine processing and discharge of gaseous and liquid radioactive wastes. Sampling and Analyses The inspectors reviewed: radioactive effluent sampling activities, representative sampling, compensatory sampling during effluent discharges with inoperable effluent radiation monitoring instrumentation, and the results of the inter-laboratory and intra-laboratory comparison program including scaling of hard-to-detect isotopes.
The inspectors conducted in-office review of the Oyster Creek 2013 and 2014 annual radioactive effluent release reports, radioactive effluent program documents, UFSAR, ODCM, and applicable event reports.
 
Walk-downs and Observations  
 
The inspectors walked down the gaseous and liquid radioactive effluent monitoring systems to assess the material condition and verify proper alignment according to plant design. The inspectors also observed potential unmonitored release points and reviewed radiation monitoring system surveillance records and the routine processing and discharge of gaseous and liquid radioactive wastes.
 
Sampling and Analyses  
 
The inspectors reviewed: radioactive effluent sampling activities, representative sampling, compensatory sampling during effluent discharges with inoperable effluent radiation monitoring instrumentation, and the results of the inter-laboratory and intra-laboratory comparison program including scaling of hard-to-detect isotopes.
 
Effluent Flow Measuring Instruments
 
The inspectors reviewed the methodology used to determine the radioactive effluent stack and vent flow rates to verify that the flow rates were consistent with technical specification, ODCM, and UFSAR values.


Effluent Flow Measuring Instruments  The inspectors reviewed the methodology used to determine the radioactive effluent stack and vent flow rates to verify that the flow rates were consistent with technical specification, ODCM, and UFSAR values.
Air Cleaning Systems


Air Cleaning Systems  The inspectors reviewed radioactive effluent discharge system surveillance test results based on technical specification acceptance criteria. Dose Calculations  The inspectors reviewed: changes in reported dose values from the previous annual radioactive effluent release reports, the scaling method for hard-to-detect radionuclides, ODCM changes, land use census changes, public dose calculations (monthly, quarterly, annual), and records of abnormal gaseous or liquid radioactive releases.
The inspectors reviewed radioactive effluent discharge system surveillance test results based on technical specification acceptance criteria.


Groundwater Protection Initiative (GPI) Implementation The inspectors reviewed: groundwater monitoring results, changes to the GPI program since the last inspection, anomalous results or missed groundwater samples, leakage or spill events including entries made into the decommissioning files (10 CFR 50.75(g)), and Exelonle results including appropriate stakeholder notifications and effluent reporting requirements. Problem Identification and Resolution The inspectors evaluated whether problems associated with the radioactive effluent monitoring and control program were identified at an appropriate threshold and properly addressed in the Exelon
Dose Calculations
 
The inspectors reviewed: changes in reported dose values from the previous annual radioactive effluent release reports, the scaling method for hard-to-detect radionuclides, ODCM changes, land use census changes, public dose calculations (monthly, quarterly, annual), and records of abnormal gaseous or liquid radioactive releases.
 
Groundwater Protection Initiative (GPI) Implementation  
 
The inspectors reviewed: groundwater monitoring results, changes to the GPI program since the last inspection, anomalous results or missed groundwater samples, leakage or spill events including entries made into the decommissioning files (10 CFR 50.75(g)),
and Exelons evaluation of any positive groundwater sample results including appropriate stakeholder notifications and effluent reporting requirements.
 
Problem Identification and Resolution  
 
The inspectors evaluated whether problems associated with the radioactive effluent monitoring and control program were identified at an appropriate threshold and properly addressed in the Exelons corrective action program.


====b. Findings====
====b. Findings====
No findings were identified.
==OTHER ACTIVITIES==
==OTHER ACTIVITIES==
{{a|4OA1}}
{{a|4OA1}}
==4OA1 Performance Indicator Verification==
==4OA1 Performance Indicator Verification==
{{IP sample|IP=IP 71151}}
{{IP sample|IP=IP 71151}}
===.1 Unplanned Scrams, Unplanned Power Changes, and Unplanned Scrams with Complications (3 samples)===
 
===.1 Unplanned Scrams, Unplanned Power Changes, and Unplanned Scrams with===
Complications===
{{IP sample|IP=IP 05000|count=3}}


====a. Inspection Scope====
====a. Inspection Scope====
cornerstone performance indicators for the period of April 1, 2014, through March 31, 2015.
The inspectors reviewed Exelons submittals for the following Initiating Events cornerstone performance indicators for the period of April 1, 2014, through March 31, 2015.
 
Unplanned Scrams
 
Unplanned Power Changes


Unplanned Scrams  Unplanned Power Changes  Unplanned Scrams with Complications To determine the accuracy of the performance indicator data reported during those periods, inspectors used definitions and guidance contained in Nuclear Energy Institute (NEI) Document 99-planning schedules, condition reports, event reports, and NRC integrated inspection reports to validate the accuracy of the submittals.
Unplanned Scrams with Complications  
 
To determine the accuracy of the performance indicator data reported during those periods, inspectors used definitions and guidance contained in Nuclear Energy Institute (NEI) Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7. The inspectors reviewed Exelons operator narrative logs, maintenance planning schedules, condition reports, event reports, and NRC integrated inspection reports to validate the accuracy of the submittals.


====b. Findings====
====b. Findings====
Line 323: Line 568:


===.2 Safety System Functional Failures (1 sample)===
===.2 Safety System Functional Failures (1 sample)===
====c. Inspection Scope====
====c. Inspection Scope====
The inspectors sampled submittals for the Safety System Functional Failures performance indicator for the period of April 1, 2014, through March 31, 2015. To determine the accuracy of the performance indicator data reported during those periods, inspectors used definitions and guidance contained in the NEI Document 99-02, 7, and NUREG-1022, reviewed operator narrative logs, operability assessments, maintenance rule records, maintenance work orders, condition reports, event reports and NRC integrated inspection reports to validate the accuracy of the submittals.
The inspectors sampled Exelons submittals for the Safety System Functional Failures performance indicator for the period of April 1, 2014, through March 31, 2015. To determine the accuracy of the performance indicator data reported during those periods, inspectors used definitions and guidance contained in the NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, and NUREG-1022, Event Reporting Guidelines 10 CFR 50.72 and 10 CFR 50.73." The inspectors reviewed Exelons operator narrative logs, operability assessments, maintenance rule records, maintenance work orders, condition reports, event reports and NRC integrated inspection reports to validate the accuracy of the submittals.


====d. Findings====
====d. Findings====
No findings were identified.  
No findings were identified.
{{a|4OA2}}
 
{{a|4OA2}}
 
==4OA2 Problem Identification and Resolution==
==4OA2 Problem Identification and Resolution==
{{IP sample|IP=IP 71152|count=1}}
{{IP sample|IP=IP 71152|count=1}}


===.1 Routine Review of Problem Identification and Resolution Activities===
===.1 Routine Review of Problem Identification and Resolution Activities===
====a. Inspection Scope====
====a. Inspection Scope====
As req the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that Exelon entered issues into the corrective action program at an appropriate threshold, gave adequate attention to timely corrective actions, and identified and addressed adverse trends. In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the corrective action program and periodically attended condition report screening meetings. The inspectors also confirmed, on a sampling basis, that, as applicable, for identified defects and non-conformances, Exelon personnel performed an evaluation in accordance with 10 CFR Part 21.
As required by Inspection Procedure 71152, Problem Identification and Resolution, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that Exelon entered issues into the corrective action program at an appropriate threshold, gave adequate attention to timely corrective actions, and identified and addressed adverse trends. In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the corrective action program and periodically attended condition report screening meetings. The inspectors also confirmed, on a sampling basis, that, as applicable, for identified defects and non-conformances, Exelon personnel performed an evaluation in accordance with 10 CFR Part 21.


====b. Findings====
====b. Findings====
Line 342: Line 587:


===.2 Semi-Annual Trend Review===
===.2 Semi-Annual Trend Review===
====a. Inspection Scope====
====a. Inspection Scope====
The inspectors performed a semi-annual review of site issues to identify trends that might indicate the existence of more significant safety concerns. As part of this review, the inspectors included repetitive or closely-related issues that may have been documented by Exelon in trend reports, site performance indicators, major equipment problem lists, system health reports, and maintenance rule assessments, and maintenance or corrective action program backlogs. The inspectors also reviewed corrective action program database for the first and second quarters of 2015 to assess condition reports written in various subject areas (equipment problems, human performance issues, etc.), as well as individual issues identified during the NRCs daily condition report review.
The inspectors performed a semi-annual review of site issues to identify trends that might indicate the existence of more significant safety concerns. As part of this review, the inspectors included repetitive or closely-related issues that may have been documented by Exelon in trend reports, site performance indicators, major equipment problem lists, system health reports, and maintenance rule assessments, and maintenance or corrective action program backlogs. The inspectors also reviewed Exelons corrective action program database for the first and second quarters of 2015 to assess condition reports written in various subject areas (equipment problems, human performance issues, etc.), as well as individual issues identified during the NRCs daily condition report review.


====b. Findings and Observations====
====b. Findings and Observations====
No findings were identified. The inspectors evaluated a sample of corrective maintenance backlogs, control room deficiency tags, open operability evaluations, and operator work-arounds. The inspectors verified that these issues were addressed within the scope of the corrective action program.
No findings were identified.


In addition, the inspectors reviewed a sampling of instrument out-of-tolerances within the last six months. The inspectors noted an apparent increase in the number of relay calibration drifts (i.e., did not meet as left condition). While a sample review by the inspectors indicated similar causal factors could not be identified, the increase in relay drifts should have warranted a more focused evaluation under station adverse rule procedures. In particular, other monitoring programs that complement the trending process, such as the instrument out-of-tolerance program, ER-AA-520, did not identify these relay malfunctions for further assessment. Exelon entered this issue into the corrective action program as issue report 2502999 for further review. The inspectors considered this a minor issue because there was not a trend of relay drifts beyond the as-found requirement specified in Technical Specifications.
The inspectors evaluated a sample of corrective maintenance backlogs, control room deficiency tags, open operability evaluations, and operator work-arounds. The inspectors verified that these issues were addressed within the scope of the corrective action program.
 
In addition, the inspectors reviewed a sampling of instrument out-of-tolerances within the last six months. The inspectors noted an apparent increase in the number of relay calibration drifts (i.e., did not meet as left condition). While a sample review by the inspectors indicated similar causal factors could not be identified, the increase in relay drifts should have warranted a more focused evaluation under station adverse rule procedures. In particular, other monitoring programs that complement the trending process, such as the instrument out-of-tolerance program, ER-AA-520, did not identify these relay malfunctions for further assessment. Exelon entered this issue into the corrective action program as issue report 2502999 for further review. The inspectors considered this a minor issue because there was not a trend of relay drifts beyond the as-found requirement specified in Technical Specifications.


{{a|4OA3}}
{{a|4OA3}}
==4OA3 Follow-Up of Events and Notices of Enforcement Discretion==
==4OA3 Follow-Up of Events and Notices of Enforcement Discretion==
{{IP sample|IP=IP 71153|count=3}}
{{IP sample|IP=IP 71153|count=3}}


===.1 Plant Events===
===.1 Plant Events===
====a. Inspection Scope====
For the plant events listed below, the inspectors reviewed and/or observed plant parameters, reviewed personnel performance, and evaluated performance of mitigating systems. The inspectors communicated the plant events to appropriate regional personnel, and compared the event details with criteria contained in IMC 0309, Reactive Inspection Decision Basis for Reactors, for consideration of potential reactive inspection activities. As applicable, the inspectors verified that Exelon made appropriate emergency classification assessments and properly reported the event in accordance with 10 CFR Parts 50.72 and 50.73. The inspectors reviewed Exelons follow-up actions related to the events to assure that Exelon implemented appropriate corrective actions commensurate with their safety significance.


====a. Inspection Scope====
RWCU system isolation due to operator error on March 26, 2015
For the plant events listed below, the inspectors reviewed and/or observed plant parameters, reviewed personnel performance, and evaluated performance of mitigating systems. The inspectors communicated the plant events to appropriate regional personnel, and compared the event details with criteria contained in IMC 0309activities. As applicable, the inspectors verified that Exelon made appropriate emergency classification assessments and properly reported the event in accordance with 10 CFR Parts 50.72 and 50.73. The inspectors reviewed  follow-up actions related to the events to assure that Exelon implemented appropriate corrective actions commensurate with their safety significance.


RWCU system isolation due to operator error on March 26, 2015  Reactor scram caused by main transformer digital protection relay system actuation on May 7, 2015
Reactor scram caused by main transformer digital protection relay system actuation on May 7, 2015


====b. Findings====
====b. Findings====
=====Introduction:=====
=====Introduction:=====
A Green self-revealing NCV of Technical Specification 6.8.1(a), because Exelon did not follow procedure system restoration on March 26, 2015. Specifically, during startup from a forced outage (1F36), Exelon did not follow procedure 303, which required correct valve lineups for system restoration of RWCU after system isolation. This resulted in decreasing reactor water level, which was automatically terminated by a second RWCU isolation.
A Green self-revealing NCV of Technical Specification 6.8.1(a),
Procedures and Programs, was identified because Exelon did not follow procedure 303, Reactor Cleanup Demineralizer System, during system restoration on March 26, 2015. Specifically, during startup from a forced outage (1F36), Exelon did not follow procedure 303, which required correct valve lineups for system restoration of RWCU after system isolation. This resulted in decreasing reactor water level, which was automatically terminated by a second RWCU isolation.


=====Description:=====
=====Description:=====
During shutdown and startup conditions, the RWCU system maintains water level in the reactor vessel to accommodate water inputs from the control rod drive system. During reactor startup and heatup activities on March 26, 2015, the RWCU system automatically isolated on high steam pressure of 136 psig (setpoint is 130 psig). The operating crew was in the process of securing the auxiliary cleanup pump and placing the main cleanup recirculating pump in service as required by procedure 201, tartup,. The operators did not complete the procedure steps in time to prevent automatic system isolation as system pressure and reactor pressure increased due to the ongoing plant startup. The inspectors determined this automatic system isolation was not more than minor because vessel level increased as a result, which was in the conservative direction. Downstream of pressure control valve (PCV) ND-11, non-regenerative heat exchanger outlet pressure control valve, system piping is rated for 150 psig and system isolations are a protective feature to prevent piping failure and draining of the reactor water through the pipe failure. With the PCV ND-11 valve full open and the increase in reactor pressure due to startup activities, the system isolated as designed. As a result   After the automatic RWCU isolation, operators implemented procedure 303, section 33, to restore letdown flow. The procedure required verification of the correct system lineup, which included: confirming PCV ND-11 was in manual mode and closed and confirming that the system inlet valve, V-16-14, was in the closed position. However, the operators did not assure PCV ND-11 was closed prior to opening V-16-14 and, as a result, drained a portion of reactor water to the condensate suction header. Reactor level dropped from , and a second automatic isolation of RWCU occurred due to the system sensing high pressure. The automatic isolation terminated the level transient.
During shutdown and startup conditions, the RWCU system maintains water level in the reactor vessel to accommodate water inputs from the control rod drive system. During reactor startup and heatup activities on March 26, 2015, the RWCU system automatically isolated on high steam pressure of 136 psig (setpoint is 130 psig).
 
The operating crew was in the process of securing the auxiliary cleanup pump and placing the main cleanup recirculating pump in service as required by procedure 201, Plant Startup, and procedure 303, Reactor Cleanup Demineralizer System. The operators did not complete the procedure steps in time to prevent automatic system isolation as system pressure and reactor pressure increased due to the ongoing plant startup. The inspectors determined this automatic system isolation was not more than minor because vessel level increased as a result, which was in the conservative direction. Downstream of pressure control valve (PCV) ND-11, non-regenerative heat exchanger outlet pressure control valve, system piping is rated for 150 psig and system isolations are a protective feature to prevent piping failure and draining of the reactor water through the pipe failure. With the PCV ND-11 valve full open and the increase in reactor pressure due to startup activities, the system isolated as designed. As a result of the isolation, reactor level rose from 158 to 172 due to loss of letdown flow.
 
After the automatic RWCU isolation, operators implemented procedure 303, section 33, Restoring RWCU after an isolation with reactor pressure greater than 125 psig, to restore letdown flow. The procedure required verification of the correct system lineup, which included: confirming PCV ND-11 was in manual mode and closed and confirming that the system inlet valve, V-16-14, was in the closed position. However, the operators did not assure PCV ND-11 was closed prior to opening V-16-14 and, as a result, drained a portion of reactor water to the condensate suction header. Reactor level dropped from approximately 172 to 153 in a short period of time, and a second automatic isolation of RWCU occurred due to the system sensing high pressure. The automatic isolation terminated the level transient.


Exelon completed an apparent cause evaluation, under issue report 2474619, and determined that the shift manager and unit supervisor shifted priority to immediately restore cleanup after the first automatic system isolation and the operators subsequently opened the V-16-14, which was not in accordance with procedure 303, section 33. The guidance in the procedure would have ensured that both V-16-14 and PCV ND-11 were in their correct lineup for the evolution and would have prevented the decrease in reactor vessel leveld enhancing operator training in system knowledge and procedure compliance and revising startup procedures.  
Exelon completed an apparent cause evaluation, under issue report 2474619, and determined that the Operations shift manager and unit supervisor shifted priority to immediately restore cleanup after the first automatic system isolation and the operators subsequently opened the V-16-14, which was not in accordance with procedure 303, section 33. The guidance in the procedure would have ensured that both V-16-14 and PCV ND-11 were in their correct lineup for the evolution and would have prevented the decrease in reactor vessel level. Exelons corrective actions included enhancing operator training in system knowledge and procedure compliance and revising startup procedures.


=====Analysis:=====
=====Analysis:=====
The failure to follow procedure 303 for restoration of RWCU after system isolation during plant startup is a performance deficiency that was reasonably within esee and correct. This finding is determined to be more than minor because it is associated with the human performance attribute of the Initiating Events cornerstone, and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, Exelon did not properly lineup the RWCU system after isolation, which resulted in a water level transient and challenging the critical safety function of inventory control.
The failure to follow procedure 303 for restoration of RWCU after system isolation during plant startup is a performance deficiency that was reasonably within Exelons ability to foresee and correct. This finding is determined to be more than minor because it is associated with the human performance attribute of the Initiating Events cornerstone, and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, Exelon did not properly lineup the RWCU system after isolation, which resulted in a water level transient and challenging the critical safety function of inventory control.
 
The inspectors evaluated the finding using IMC 0609.04, Initial Characterization of Findings, and IMC 0609, Appendix A, Exhibit 1, Initiating Events Screening Questions.
 
The inspectors determined that this finding is a transient initiator that did not cause a reactor trip and loss of mitigation equipment relied upon to transition the plant from the onset of the trip to a stable shutdown condition. Therefore, the inspectors determined the finding to be of very low safety significance (Green).


The inspectors evaluated the finding using  The inspectors determined that this finding is a transient initiator that did not cause a reactor trip and loss of mitigation equipment relied upon to transition the plant from the onset of the trip to a stable shutdown condition. Therefore, the inspectors determined the finding to be of very low safety significance (Green). This finding has a cross-cutting aspect in the area of Human Performance, Challenge the Unknown, because Exelon did not recognize and plan for the possibility of mistakes, or implement appropriate error reduction tools. Specifically, the operators did not stop and fully communicate plant condition after the initial RWCU isolation. Consequently, operators opened the RWCU system inlet valve due to the increasing water level without following procedure guidance. [H.11]  
This finding has a cross-cutting aspect in the area of Human Performance, Challenge the Unknown, because Exelon did not recognize and plan for the possibility of mistakes, or implement appropriate error reduction tools. Specifically, the operators did not stop and fully communicate plant condition after the initial RWCU isolation. Consequently, operators opened the RWCU system inlet valve due to the increasing water level without following procedure guidance. [H.11]  


=====Enforcement:=====
=====Enforcement:=====
part, that written procedures shall be established, implemented and maintained covering the applicable procedures recommended in Appendix A of Regulatory Guide 1.33, Revision 2. Regulatory Guide 1.33, Appendix A, requires that safety related activities listed be covered in written procedures such as the reactor cleanup system. Contrary to the above, on March 26, 2015, Exelon did not properly implement the reactor cleanup system procedure. Specifically, Exelon did not follow procedure 303, section 33, RWCU after isolation with reactor pressure greater than 125 psig. As a result, reactor water level decreased approximately twenty inches in a short period of d enhancing operator training in system knowledge and procedure compliance and revising startup procedures. Because this violation is corrective action program as issue report 2474619, this violation is being treated as an NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy. (NCV 05000219/2015002-03, Reactor Water Cleanup Procedure Not Followed Resulting in a Level Transient)
Technical Specification 6.8.1(a), Procedures and Programs, states, in part, that written procedures shall be established, implemented and maintained covering the applicable procedures recommended in Appendix A of Regulatory Guide 1.33, Revision 2. Regulatory Guide 1.33, Appendix A, requires that safety related activities listed be covered in written procedures such as the reactor cleanup system. Contrary to the above, on March 26, 2015, Exelon did not properly implement the reactor cleanup system procedure. Specifically, Exelon did not follow procedure 303, section 33, Restoring RWCU after isolation with reactor pressure greater than 125 psig. As a result, reactor water level decreased approximately twenty inches in a short period of time. Exelons corrective actions included enhancing operator training in system knowledge and procedure compliance and revising startup procedures. Because this violation is of very low safety significance (Green) and was entered into Exelons corrective action program as issue report 2474619, this violation is being treated as an NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy. (NCV 05000219/2015002-03, Reactor Water Cleanup Procedure Not Followed Resulting in a Level Transient)


===.2 (Closed) Licensee Event Report (LER) 05000219/2014-006-00:===
===.2 (Closed) Licensee Event Report (LER) 05000219/2014-006-00:===
Reactor SCRAM due to Decreasing Water Level On October 12, 2014, during a plant startup from a refueling outage (1R25), and reactor power ascension at approximately 1 percent of rated thermal power, reactor water level began to lower. An automatic reactor scram occurred moments before operators inserted a manual scram in accordance with station procedures. Following the reactor scram, all systems operated as expected. At the time of the event, Exelon personnel were performing a post- Exelon personnel reset  the AVR controllers, which triggered logic to trip the turbine.
Reactor SCRAM due to Decreasing Water Level  


Exelon performed a root cause analysis on the event and determined station leadership inconsistently reinforced human performance error reduction, tool use, and procedure use and adherence. Exelon has taken steps to reduce these weaknesses in the future, which included the establishment of a performance improvement action plan focused on the human performance fundamentals. The inspectors determined there was a self-revealing finding during the review of the LER (see below). This LER is closed.
On October 12, 2014, during a plant startup from a refueling outage (1R25), and reactor power ascension at approximately 1 percent of rated thermal power, reactor water level began to lower. An automatic reactor scram occurred moments before operators inserted a manual scram in accordance with station procedures. Following the reactor scram, all systems operated as expected. At the time of the event, Exelon personnel were performing a post-maintenance test on the AVRs HMI. Exelon personnel reset the AVR controllers, which triggered logic to trip the turbine.
 
Exelon performed a root cause analysis on the event and determined station leadership inconsistently reinforced human performance error reduction, tool use, and procedure use and adherence. Exelon has taken steps to reduce these weaknesses in the future, which included the establishment of a performance improvement action plan focused on the human performance fundamentals.
 
The inspectors determined there was a self-revealing finding during the review of the LER (see below). This LER is closed.


====a. Findings====
====a. Findings====
.  
.


=====Introduction.=====
=====Introduction.=====
A self-revealing Green finding was identified because Exelon did not properly screen work in accordance with MA-AA-716-Specifically, on September 12, 2014, Exelon did not screen the HMI post-maintenance test per the maintenance planning procedure. As a result, on October 12, 2014, Exelon personnel performing the post-maintenance test did not have a work order, which would have included plant configurations and limitations associated with the test. This led to an automatic reactor scram.
A self-revealing Green finding was identified because Exelon did not properly screen work in accordance with MA-AA-716-010, Maintenance Planning.
 
Specifically, on September 12, 2014, Exelon did not screen the AVRs HMI post-maintenance test per the maintenance planning procedure. As a result, on October 12, 2014, Exelon personnel performing the post-maintenance test did not have a work order, which would have included plant configurations and limitations associated with the test.
 
This led to an automatic reactor scram.


=====Description.=====
=====Description.=====
On October 12, 2014, while the plant was at approximately 1 percent power during plant startup following refueling outage (1R25), a reactor scram occurred due to low level in the reactor vessel.
On October 12, 2014, while the plant was at approximately 1 percent power during plant startup following refueling outage (1R25), a reactor scram occurred due to low level in the reactor vessel.


following issues with the software. The purpose of the AVR is to regulate main generator output voltage. A contractor was tasked to perform a post-maintenance test following the troubleshooting to ensure the HMI was properly communicating with the   During the post-maintenance test, the contractor recognized that the HMI was communicating with the M2 controller but not the M1 controller. At this point, the contractor should have stopped work and noted the deviation from the expected result as a failed post-maintenance test. However, the contractor directed the electrical technician to continue work and reset the M1 controller. This action did not restore communication between the AVR and HMI. The contractor then directed the electrical technician to reset all three AVR controllers:  M1, M2, and C. The reset of the three AVR controllers triggered the logic to trip the turbine. The reactor protection system received a reactor low level signal, which caused an automatic reactor scram. The plant responded as expected.
A portion of the outage scope was to troubleshoot and repair the AVRs HMI computer following issues with the software. The purpose of the AVR is to regulate main generator output voltage. A contractor was tasked to perform a post-maintenance test following the troubleshooting to ensure the HMI was properly communicating with the AVR controllers per Exelon procedure 421, EX2100e HMI, Trouble and Fault Alarms.


On September 12, 2014, when Exelon added this activity into the scope of the outage, Exelon personnel did not properly screen the work activity to determine if the post-maintenance test required a work order per MA-AA-716-Instead, the activity was performed under an action request, which did not include requirements for precautions and limitations, and a pre-job brief was not performed. Per MA-AA-716-010, the work was required to be a Level 1 activity due to the location and work to be performed. Specifically, table 2 in MA-AA-716--maintenance testing work activity performed in the power block requires a Level 1 or Level 2 work package. MA-AA-716-010, ing Decision Tree -maintenance testing in the power block that is complex or infrequently performed requires a Level 1 work package. MA-AA-716-Had the post-maintenance test been properly categorized as an infrequent activity, according to MA-AA-716-010, a Level 1 activity would require a detailed work package. Per  MA-AA-716-010, Attachment 6, a detailed work package states minimum expected content to include, in part, precautions and limitations and a pre-job brief. Exelon -AA-716-010, A-AA-716-  Per HU-AA---job briefings are conducted for low risk, infrequent activities and include contingencies and stop-work criteria. If a pre-job brief had been performed, it should have discussed Exelon personnel actions if the HMI failed to respond as expected. A proper work package should have provided barriers to prevent Exelon from working beyond the scope of the post-maintenance test such as following a stop-work criteria.
During the post-maintenance test, the contractor recognized that the HMI was communicating with the M2 controller but not the M1 controller. At this point, the contractor should have stopped work and noted the deviation from the expected result as a failed post-maintenance test. However, the contractor directed the electrical technician to continue work and reset the M1 controller. This action did not restore communication between the AVR and HMI. The contractor then directed the electrical technician to reset all three AVR controllers: M1, M2, and C. The reset of the three AVR controllers triggered the logic to trip the turbine. The reactor protection system received a reactor low level signal, which caused an automatic reactor scram. The plant responded as expected.


HU-AA- in part, personnel should stop if they find themselves outside of procedures, parameters, or processes when unexpected post-maintenance test results are received. Attachment 4 of HU-AA-101 defines one example of stop-work criteria as a work performance issues, specifically equipment that does not respond as expected. Had HU-AA-101 been implemented, Exelon personnel should have stopped the post-maintenance test when the HMI screen did not respond as expected, thus preventing the automatic reactor scram.  
On September 12, 2014, when Exelon added this activity into the scope of the outage, Exelon personnel did not properly screen the work activity to determine if the post-maintenance test required a work order per MA-AA-716-010, Maintenance Planning.
 
Instead, the activity was performed under an action request, which did not include requirements for precautions and limitations, and a pre-job brief was not performed. Per MA-AA-716-010, the work was required to be a Level 1 activity due to the location and work to be performed. Specifically, table 2 in MA-AA-716-010 Work Package Usage Based on Type of Work Activity and Location, states, in part, a post-maintenance testing work activity performed in the power block requires a Level 1 or Level 2 work package. MA-AA-716-010, Attachment 6, Graded Approach to Planning Decision Tree for Work Package Level Determination, states in part, post-maintenance testing in the power block that is complex or infrequently performed requires a Level 1 work package.
 
MA-AA-716-010 defines infrequent as greater than 12 months. Had the post-maintenance test been properly categorized as an infrequent activity, according to MA-AA-716-010, a Level 1 activity would require a detailed work package. Per MA-AA-716-010, Attachment 6, a detailed work package states minimum expected content to include, in part, precautions and limitations and a pre-job brief. Exelon completed a root cause evaluation, which stated, in part, Per MA-AA-716-010, Maintenance Planning, and MA-AA-716-235, Control of Critical Digital Asset Portable Media and Portable Devices, a work order was required for this activity.
 
Per HU-AA-1211, Pre-job Briefings, standard pre-job briefings are conducted for low risk, infrequent activities and include contingencies and stop-work criteria. If a pre-job brief had been performed, it should have discussed Exelon personnel actions if the HMI failed to respond as expected. A proper work package should have provided barriers to prevent Exelon from working beyond the scope of the post-maintenance test such as following a stop-work criteria.
 
HU-AA-101, Human Performance Tools and Verification Practices, Step 4.1.3 states, in part, personnel should stop if they find themselves outside of procedures, parameters, or processes when unexpected post-maintenance test results are received. Attachment 4 of HU-AA-101 defines one example of stop-work criteria as a work performance issues, specifically equipment that does not respond as expected. Had HU-AA-101 been implemented, Exelon personnel should have stopped the post-maintenance test when the HMI screen did not respond as expected, thus preventing the automatic reactor scram.


=====Analysis.=====
=====Analysis.=====
The failure to properly screen the HMI work per MA-AA-716-010 is a finding is determined to be more than minor because it is associated with the human performance attribute of the Initiating Events cornerstone and affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during power operation. Specifically, resetting the three AVR controllers caused an automatic reactor scram. The inspectors evaluated the finding using IMC Initiating Events Screening Questions The inspectors determined that this finding was a transient initiator that did not cause a reactor trip and loss of mitigation equipment relied upon to transition the plant from the onset of the trip to a stable shutdown condition. Therefore, the inspectors determined the finding to be of very low safety significance (Green).
The failure to properly screen the HMI work per MA-AA-716-010 is a performance deficiency that was within Exelons ability to foresee and correct. This finding is determined to be more than minor because it is associated with the human performance attribute of the Initiating Events cornerstone and affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during power operation. Specifically, resetting the three AVR controllers caused an automatic reactor scram. The inspectors evaluated the finding using IMC 0609.04, Initial Characterization of Findings, and IMC 0609, Appendix A, Exhibit 1, Initiating Events Screening Questions. The inspectors determined that this finding was a transient initiator that did not cause a reactor trip and loss of mitigation equipment relied upon to transition the plant from the onset of the trip to a stable shutdown condition. Therefore, the inspectors determined the finding to be of very low safety significance (Green).


This finding has a cross cutting aspect in the area of Human Performance associated with Challenge the Unknown, because Exelon personnel did not stop when faced with uncertain situations. Specifically, on October 12, 2014, Exelon personnel did not stop when faced with the uncertain situation of the HMI screen not responding as expected. [H.11]
This finding has a cross cutting aspect in the area of Human Performance associated with Challenge the Unknown, because Exelon personnel did not stop when faced with uncertain situations. Specifically, on October 12, 2014, Exelon personnel did not stop when faced with the uncertain situation of the HMI screen not responding as expected.
 
[H.11]  


=====Enforcement.=====
=====Enforcement.=====
This finding does not involve enforcement action because no violation of regulatory requirements violation was identified. Exelon entered this issue into their corrective action program as issue report 2394374. Because this issue does not involve a violation and has very low safety significance, it is identified as a finding. (FIN 05000219/2015002-04, Reset of the Automatic Voltage Regulator Controllers Led to an Automatic Reactor Scram)  
This finding does not involve enforcement action because no violation of regulatory requirements violation was identified. Exelon entered this issue into their corrective action program as issue report 2394374. Because this issue does not involve a violation and has very low safety significance, it is identified as a finding. (FIN 05000219/2015002-04, Reset of the Automatic Voltage Regulator Controllers Led to an Automatic Reactor Scram)  
 
{{a|4OA6}}
{{a|4OA6}}
==4OA6 Meetings, Including Exit==
==4OA6 Meetings, Including Exit==
On July 10, 2015, the inspectors presented the inspection results to Mr. G. Stathes, Site Vice President, and other members of the Oyster Creek staff. The inspectors verified that no proprietary information was retained by the inspectors or documented in this report.
On July 10, 2015, the inspectors presented the inspection results to Mr. G. Stathes, Site Vice President, and other members of the Oyster Creek staff. The inspectors verified that no proprietary information was retained by the inspectors or documented in this report.
Line 416: Line 692:


==KEY POINTS OF CONTACT==
==KEY POINTS OF CONTACT==
Exelon Personnel
Exelon Personnel  
: [[contact::G. Stathes]], Site Vice President  
: [[contact::G. Stathes]], Site Vice President  
: [[contact::J. Dostal]], Plant Manager  
: [[contact::J. Dostal]], Plant Manager  
: [[contact::M. Ford]], Director, Operations
: [[contact::M. Ford]], Director, Operations  
: [[contact::J. Stanley]], Director, Engineering  
: [[contact::J. Stanley]], Director, Engineering  
: [[contact::D. Chernesky]], Director, Maintenance  
: [[contact::D. Chernesky]], Director, Maintenance  
Line 425: Line 701:
: [[contact::D. DiCello]], Director, Work Management  
: [[contact::D. DiCello]], Director, Work Management  
: [[contact::M. McKenna]], Manager, Regulatory Assurance  
: [[contact::M. McKenna]], Manager, Regulatory Assurance  
: [[contact::T. Farenga]], Radiation Protection Manager
: [[contact::T. Farenga]], Radiation Protection Manager  
: [[contact::J. Renda]], Manager, Environmental/Chemistry  
: [[contact::J. Renda]], Manager, Environmental/Chemistry  
: [[contact::T. Keenan]], Manager, Site Security  
: [[contact::T. Keenan]], Manager, Site Security  
Line 434: Line 710:
: [[contact::K. Wolfe]], Manager, Health Physics  
: [[contact::K. Wolfe]], Manager, Health Physics  
: [[contact::J. McCarthy]], Senior Radiological Engineer  
: [[contact::J. McCarthy]], Senior Radiological Engineer  
: [[contact::M. Nixon]], Chemist RETS/REMP  
: [[contact::M. Nixon]], Chemist - RETS/REMP  
: [[contact::J. Eagan]], Manager, Operations Training  
: [[contact::J. Eagan]], Manager, Operations Training  
: [[contact::G. Young]], LORT Exam Author  
: [[contact::G. Young]], LORT Exam Author  
: [[contact::J. Gessner]], LORT Exam Author  
: [[contact::J. Gessner]], LORT Exam Author  
: [[contact::M. Rossi]], LORT Lead  
: [[contact::M. Rossi]], LORT Lead  
 
==LIST OF ITEMS OPENED, CLOSED, DISCUSSED, AND UPDATED==
==LIST OF ITEMS OPENED, CLOSED, DISCUSSED, AND UPDATED==
===Opened/Closed===
===Opened/Closed===
: 05000219/2015002-01 FIN Inadequate Assessment of 4k Emergency Switchgear Roll-Up Door Degraded Floor Gasket (Section 1R06)  
: 05000219/2015002-01 FIN Inadequate Assessment of 4k Emergency Switchgear Roll-Up Door Degraded Floor Gasket (Section 1R06)  
: 05000219/2015002-02 FIN Failure Rates Exceed Twenty Percent for Annual Requalification Exam (Section 1R11)
: 05000219/2015002-02 FIN Failure Rates Exceed Twenty Percent for Annual Requalification Exam (Section 1R11)  
: 05000219/2015002-03 NCV Reactor Water Cleanup Procedure Not Followed Resulting in a Level Transient (Section 4OA3)
: 05000219/2015002-03 NCV Reactor Water Cleanup Procedure Not Followed Resulting in a Level Transient (Section 4OA3)  
: 05000219/2015002-04 FIN Reset of the Automatic Voltage Regulator Controller Led to an Automatic Reactor Scram (Section 4OA3)    
: 05000219/2015002-04 FIN Reset of the Automatic Voltage Regulator Controller Led to an Automatic Reactor Scram (Section 4OA3)  


===Closed===
===Closed===
: [[Closes LER::05000219/LER-2014-006]]-00 LER Reactor SCRAM Due to Decreasing Water Level (Section 4OA3)  
: 05000219/2014-006-00 LER Reactor SCRAM Due to Decreasing Water Level (Section 4OA3)  
 
==LIST OF DOCUMENTS REVIEWED==
==LIST OF DOCUMENTS REVIEWED==
==Section 1R01: Adverse Weather Protection==
===Procedures===
: ABN 60, Grid Emergency, Revision 15 310, Containment Spray System Operation, Revision 110 341, Emergency Diesel Generator Operation, Revision 109
: EN-OC-402-0005, Extreme Heat Implementation Plan, Revision 0
: OP-OC-108-109-1001, Severe Weather Preparation T&RM for Oyster Creek, Revision 30
: OP-AA-108-111-1001, Severe Weather and Natural Disaster Guidelines, Revision 12
===Condition Reports===
: 2505124
: 2505007
: 2503374
: 2493587
: 2490313
: 2479505
: 2485242
: 2485345
: 1462889
: 1250934
: 1650001
: 1673984
: 1697151
: 2426971
: 1619952
: 1649628
: 1674151
: 1681139
: 2438931
: 2448636
: 2457139
: 2439068
: 2438853
: Maintenance Orders/Work Orders
: C2033397 R2234027
==Section 1R04: Equipment Alignment==
===Procedures===
: 304, Standby Liquid Control System Operation, Revision 48 309.1, Turbine Building Closed Cooling Water System, Revision 57
: 307, Isolation Condenser System, Revision 124 341, Emergency Diesel Generator Operation, Revision 108
===Drawings===
: BR 2005, Emergency Service Water System Flow Diagram, Revision 86
: BR 2006, Turbine Building Closed Cooling Water Flow Diagram, Sheet 5, Revision 59
==Section 1R05: Fire Protection==
===Procedures===
: OP-OC-201-008, Oyster Creek Pre-Fire Plans, Revision 18
: OP-OC-201-012-1001, On-Line Fire Risk Management, Revision 3
: OP-AA-201-012-1001, Operations On-Line Fire Risk Management, Revision 1
: OP-AA-108-117, Protected Equipment Program, Revision 4
: WC-AA-101-1006, On-Line Risk Management and Assessment, Revision 1
: ER-AA-600-1069, High Risk Fire Area Identification, Revision 1
: OP-OC-201-008-1029, Feed Pump Room, Revision 1
: OP-OC-201-008-1027, Turbine Building Basement South, Revision 2
: OP-OC-201-008-1020, Cable Spreading Room, Revision 1
: RAP-LFAP5 (2-d), Alarm Silence, Revision 0
: RAP-LFAP5 (6-b), LFAPS Battery Trouble, Revision 1
: OP-OC-201-008-1036, Emergency Diesel Generator Room #2, Revision 2
: OP-OC-201-008-1008, Reactor Building (-
: OP-OC-201-008-1009, Reactor Building (-
==Section 1R06: Flood Protection Measures==
===Procedures===
: OP-AA-108-115, Operability Determinations, Revision 16
: OP-AA-108-115-1002, Supplemental Consideration for On-Shift Immediate Operability
: Determinations, Revision 3 101.2, Oyster Creek Site Fire Protection Program, Revision 73
: ER-AA-300-150, Cable Condition Monitoring Program, Revision 0
: MA-OC-773-001, Testing/Condition Monitoring of Inaccessible Medium Voltage Cables Not
: Subject to 10
: CFR 50.49 Environmental Qualification, Revision 1 2400-SMM-3572.01, Reactor Building Sump Isolation Valve Leak Rate Test, Revision 2
: EMG 3200.11, Secondary Containment Control, Revision 8
: RAP-RB1C (1-7), 1-7 Sump Reactor Building Floor Drain Sump High Level, Revision 1
===Drawings===
: GE 157B6350, Reactor Building Floor and Equipment Drains Electrical Elementary Diagram,
: Sheet 55C, Revision 5
: GE 157B6350, Reactor Building Floor and Equipment Drains Electrical Elementary Diagram,
: Sheet 55D, Revision 5 3C-572-17-1000, Reactor Building Floor and Equipment Drains Electrical Elementary Diagram,
: Sheet 0, Revision 0
: JC 147434, Sumps and Waste Collection System, Sheet 3, Revision 68
===Condition Reports===
: 2484452
: 2484454
: 1503499
: 1430624
: 2383723
: 2493515
: 2411241
: 2491855
: 2491672
: 2492094
: 1537101
: 1537254
: 1553547
: 1566391
: 1636369
: 2491584
: 2491855
: 2507389
: 2423574
: 0813797
: Maintenance Orders/Work Orders
: C2029700 R2219628 R2121522 R2136655 R2181319 R0803021 R2245139 R2215948 R2249794
===Miscellaneous===
: HVA TD Report Summary: 86-71 Left Conduit, dated September 19, 2014 HVA TD Report Summary: 86-71 Right Conduit, dated September 19, 2014 Design and Licensing Bases for Flooding at OCGS, dated August 29, 2007 Oyster Creek Nuclear Generating Station Updated Final Safety Analysis Report Section 9.3, Process Auxiliaries, Revision 16
: OC-PSA-012, Internal Flood Evaluation Summary Notebook, Revision 1
==Section 1R07: Heat Sink Performance==
===Procedures===
: ER-OC-340-1001, Oyster Creek Generic Letter 89-13 Program Basis Document, Revision 4
: ER-AA-340-1002, SW Heat Exchanger and Component Inspection Guide, Revision 6 309.2, Reactor Building Closed Cooling Water System, Revision 93
===Condition Reports===
: 2468541
: 2470660
: Maintenance Orders/Work Orders R2237112
===Miscellaneous===
: VM-OM-0354, Installation, Operation, and Maintenance for the Reactor Building Closed Cooling
: Water Heat Exchanger, Revision 1
==Section 1R11: Licensed Operator Requalification Program==
===Procedures===
: 203, Plant Shutdown, Revision 85 203.4, Plant Cooldown Following Reactor Scram, Revision 55
: HU-AA-1211, Pre-Job Briefings, Revision 9
: OP-AA-105-102, NRC Active License Maintenance, Revision 11
: TQ-AA-150, Operator Training Programs, Revision 11
: TQ-AA-155, Conduct of Simulator Training and Evaluation, Revision 4
: TQ-AA-155, Conduct of Simulator Training and Evaluation, Revision 4
: TQ-AA-201, Examination Security and Administration, Revision 16
: TQ-AA-224, Implementation Phase, Revision 8
===Condition Reports===
: 2477483
: 2497537
: 2474619
: 2513013
: Job Performance Measures
: 345.05A 200.10A 212.05
: 279.06
: 288.05
: 264.06 345.08A 200.17A 279.03
: 207.06
: 202.16
: 204.12A
: Comprehensive Written Exams
: LORT- LORT-
: Simulator Scenarios
: 2010-51 2010-52 2010-53 2010-54 2010-56 2010-60
: 2010-62
: Simulator Testing
: 75% Steady State Accuracy Test, 12/31/14, Revision 1 Manual Reactor Scram, 1/31/15, Revision 14 Simultaneous Closure of all MSIVs, 1/31/15, Revision 13 Simultaneous Trip of All Five Recirculation Pumps, 1/31/15, Revision 10 LOCA with Loss of Offsite Power, 1/31/15, Revision 14 
: Maximum Size Unisolable Main Stream Line Rupture, 3/4/15, Revision 12 Trip of a Single Recirculation Pump, 3/15/15, Revision 13 Maximum Rate Power Ramp from 100% to 75%, 3/22/15, Revision 13
==Section 1R12: Maintenance Effectiveness==
===Procedures===
: ER-AA-310, Implementation of the Maintenance Rule, Revision 9
: ER-AA-310-1001, Maintenance Rule
: Scoping, Revision 4
: ER-AA-310-1003, Maintenance Rule
: Performance Criteria Selection, Revision 4
: ER-AA-310-1004, Maintenance Rule
: Performance Monitoring, Revision 13 308, Emergency Core Cooling System Operation, Revision 95
===Condition Reports===
: 2494063
==Section 1R13: Maintenance Risk Assessments and Emergent Work Control==
===Procedures===
: 307, Isolation Condenser System, Revision 124
: WC-AA-101, Online Work Control Process, Revision 24
: WC-AA-104, Integrated Risk Management, Revision 17
: OP-AA-108-117, Protected Equipment Program, Revision 2
: WC-OC-101-1001, Online Risk Management and Assessment, Revision 18
: ER-AA-600-1042, Online Risk Management
: 322, Service Water System, Revision 85
: 341, Emergency Diesel Generator Operation, Revision 108
: 309.2, Reactor Building Closed Cooling Water System, Revision 93
==Section 1R15: Operability Determinations and Functionality Assessments==
===Procedures===
: 304, Standby Liquid Control System Operation, Revision 48 322., Service Water System, Revision 85 612.4.001, Standby Liquid Control Pump and Valve Operability and In-Service Test, Revision 49 612.4.002, Standby Liquid Control System Functional Test, Revision 36 ABN 5, Inadvertent SLC Initiation, Revision 5 308, Emergency Core Cooling System Operation, Revision 95 610.4.021, Core Spray System 1 Pump Operability and Quarterly In-Service Test, Revision 29
: ER-AA-321, Administrative Requirements for Inservice Testing, Revision 12
: HU-AA-104-101, Procedure Use and Adherence, Revision 5
===Drawings===
: BR2005, Emergency Service Water System Flow Diagram, Revision 86 GE148F723, Liquid Poison System Flow Diagram, Revision 40
===Calculations===
: C-1302-212-E540-100, OCNGS: LPCS Single Pump Operability Criteria, Revision 1
: C-1302-212-5310-091, OCNGS: LPCS Operability Criteria, Revision 1
: C-1302-241-E540-096, OCNGS Containment Spray/Emergency Service Water System Hydraulic Models, Revision 2
===Condition Reports===
: 1421400
: 2476604
: 2386417
: 2456720
: 1336412
: 0698203
: 1122927
: 1083669
: 2452480
: 1352614
: 1466639
: 1422090
: 2489885
: 2514081
: Maintenance Orders/Work Orders R2251968 R2221605 R2215329 A2185795 M2371508
===Miscellaneous===
: Operability Evaluation
: OC-2005-OE-0002, Revision 1
: VM-OC-2036, Installation, Operation & Maintenance for Bladder Accumulator (Liquid Poison System), Revision 2 Oyster Creek Nuclear Generating Station Updated Final Safety Analysis Report Section 9.3, Process Auxiliaries, Revision 18
: Oyster Creek Nuclear Generating Station Technical Specifications Section 3.2, Reactivity Control, Amendment 262
: P-20-2A (NZ3A) & P-20-2C (NZ3C) IST Pump Evaluation Form, Dated May 27, 2015
: Safety Evaluation 000212-036, Core Spray System Operability Criteria Review, Revision 0
: Safety Evaluation 000212-046, Core Spray System Main Pump Operability Criteria, Revision 0
: Oyster Creek Nuclear Generating Station Updated Final Safety Analysis Report Section 6.3, Emergency Core Cooling System, Revision 18
: OC 01-00621, Crosstie ESW to Service Water to Allow Repairs, Revision 0
: OC 08-00037, UFSAR Update for ESW Cross-Connect to SW for RBCCW, Revision 0
: OC 09-00433, Service Water Cross Connect from RBCCW Ht Exch to ESW sys 1, Revision 0
: VM-OC-2773, Wafer Sphere Valves for Service Water/ESW Crosstie, Revision 0
: OC-2008-E-0001, Technical Evaluation A2185795-02, Revision 0
==Section 1R18: Plant Modifications==
===Procedures===
: 619.4.025, Automatic Scram Contactor Test, Revision 13
: ER-AA-600-1051, Risk Assessment of Surveillance Test Frequency Changes, Revision 0
: ER-AA-425, Implementation of the Technical Specification Surveillance Frequency Control Program, Revision 1
: ER-AA-425-1000, Selecting a Candidate to be Evaluated for a Proposed Surveillance Test Interval (STI) Change, Revision 1
: ER-AA-4225-1001, Surveillance Test Interval (STI) Evaluation Form, Revision 0
: ER-AA-425-1002, Engineering Evaluation of Proposed Surveillance Test Interval Changes, Revision 1
: ER-AA-600-1051, Risk Assessment of Surveillance Test Frequency Changes, Revision 0
: LS-AA-1000, Surveillance Frequency Control Program List of Surveillance Frequencies Change Process, Revision 0
: LS-AA-104-1000, 50.59 Resource Manual, Revision 9
: LS-AA-104, Exelon 50.59 Review Process, Revision 10
: LS-AA-104-1003, 50.59 Screening Form, Revision 4
===Condition Reports===
: 1619815
: 1685273
: 1473196
: 1494974 
: Maintenance Orders/Work Orders R2132226 R2245216
===Miscellaneous===
: STI
: OC-15-01, Automatic Scram Contactor Surveillance Extension, Revision 0
: TCC-1504-532-RO-22, ESW I/SW Cross Connect Restriction Orifice, Revision 0
: OC 01-00621, Crosstie ESW to Service Water to Allow Repairs, Revision 0
: OC 08-00037, UFSAR Update for ESW Cross-Connect to SW for RBCCW, Revision 0
: OC 09-00433, Service Water Cross Connect from RBCCW Ht Exch to ESW sys 1, Revision 0
: VM-OC-2773, Wafer Sphere Valves for Service Water/ESW Crosstie, Revision 0
: OC-2008-E-0001, Technical Evaluation A2185795-02, Revision 0
: OC 15-00197, ECR to Remove the Output Trip Functions from the Digital Protection Relay System, Revision 0
==Section 1R19: Post-Maintenance Testing==
===Procedures===
: MA-AA-716-012, Post Maintenance Testing, Revision 20
: WC-AA-101, On-Line Work Control Process, Revision 24
: MA-AA-716-011, Work Execution & Close Out, Revision 19 2400-GMM-3225.52, Control Rod Drive Hydraulic Control Unit, Revision 34
: 235, Determination and Correction of Control Rod Drive System Problems, Revision 65
: 607.4.005, Containment Spray and Emergency Service Water Pump System 2 Operability  and Comprehensive/Preservice/Post Maintenance Inservice Test, Revision 78
: 617.4.002, CRD Exercise and Flow Test/IST Cooling Water Header Check Valve, Revision 67 341, Emergency Diesel Generator Operation, Revision 109
: 636.4.013, Diesel Generator #2 Load Test, Revision 45
: 635.2.005, Main Generator and Main Transformer Bank 1 Protective Relay Surveillance, Revision 10
: RAP-R5a, MN Field Brkr Trip, Revision 0
: RAP-R3d, Lockout Relay Trip, Revision 2
===Drawings===
: GE 197E871, Scram Discharge Volume System Control Rod Drive Hydraulic System, Sheet 1, Revision 30 GU 3D-711-17-1004, Main Gen Protect Relays Electrical Elementary Diagram Main Transformer Lock-Out Relay 86T, Revision 4
: GE 991D0217, Main Generator Electrical Elementary Diagram Relaying and Metering Three Line, Revision 35
===Calculations===
: C-1302-532-E540-036, ESW System Performance with Keepfill Line Failure, Revision 2
: Maintenance Orders/Work Orders
: C2034201
: C2033513 R2226691 R2256758
===Miscellaneous===
: Oyster Creek Nuclear Generating Station Updated Final Safety Analysis Report Section 4.6, Functional Design of Reactivity Control Systems, Revision 14
: OC 15-00197, ECR to Remove the Output Trip Functions from the Digital Protection Relay System, Revision 0
==Section 1R20: Refueling and Other Outage Activities==
===Procedures===
: 305, Shutdown Cooling System Operation, Revision 121
: 203.4, Plant Cooldown Following Reactor Scram, Revision 55
: OP-AA-108-114, Post Transient Review, Revision 11
: OP-AA-108-108, Unit Restart Review, Revision 16
: 201, Plant Startup, Revision 97
: ABN-1, Reactor Scram, Revision 13
: ABN-2, Recirculation System Failures, Revision 24
: ABN-10, Turbine Generator Trip, Revision 14
===Condition Reports===
: 2500906
: 2500895
: 2500776
: 2500586
: 2500426
: 2500401
: 2500317
: 2499907
: 2499810
: 2499768
: 2497537
===Miscellaneous===
: Oyster Creek Nuclear Generating Station Updated Final Safety Analysis Report, Section 10.2, Turbine Generator, Revision 19
: ECR 15-00197, ECR to Remove the Main Transformer Differential Current Trip from the Digital Protection Relay System (DPRS), Revision 0
: ODM
: 1F37 Startup Without Identifying Cause of Main Transformer Differential PTR
: 2497537, Post Transient Review, Revision 0
==Section 1R22: Surveillance Testing==
===Procedures===
: 307, Isolation Condenser System, Revision 121
: 609.3.022, A Isolation Condenser Isolation Test and Calibration
: A1 Sensors First, Revision 4
: 609.4.001, Isolation Condenser Valve Operability and In Service Test, Revision 80
: 609.3.012, Isolation Condenser Isolation Test and Calibration
: A2 Sensors First, Revision 16
: 609.3.013, Isolation Condenser Isolation Test and Calibration
: B2 Sensors First, Revision 6
: 609.3.022, A Isolation Condenser Isolation Test and Calibration
: A1 Sensors First, Revision 5
: 609.3.023, B Isolation Condenser Isolation Test and Calibration
: B1 Sensors First, Revision 5
: 312.9, Primary Containment Control, Revision 58
: ER-AB-331-1006, BWR Reactor Coolant System Leakage Monitoring and Action Plan,
: Revision 2
: 610.4.003, Core Spray Valve Operability and In-Service Test, Revision 44
: EN-OC-300-1001, Oyster Creek MOV
: GL 89-10 Scoping Document, Revision 3
===Drawings===
: GE 237E487, Control Rod Drive System Flow Diagram, Sheet 1, Revision 68
: GE 148F262, Emergency Condenser Flow Diagram, Sheet 1, Revision 51
===Calculations===
: C-1302-211-5350-080, Timer Setpoint Uncertainty, Revision 1
: C-1302-730-5350-017, Stroke Time Calculation for
: GL 89-, Revision 0
===Condition Reports===
: 2478140
: 2494991
: 2495022
: 2494966
: 2492268
: 2477387
: 2476241
: 2475784
: 2476241
: 2475490
: 2478172
: 2475658
: 2508916
: 2511400
: 2513941
: 2509739
: 2497353
: 2478140
: 1497655
: 2498892
: Maintenance Orders/Work Orders R2247065 R2241124 R2253286 R2254595
: C2034491
: C2034492
===Miscellaneous===
: VM-OC-0285, ITT Barton Model 580 A-0 DPIS, Revision 5
: VM-OC-5001, Care and Operation of Isolation Condensers, Revision 3
: Oyster Creek Nuclear Generating Station Technical Specifications Section 3.8, Isolation Condenser, Amendment 241
: Oyster Creek Nuclear Generating Station Updated Final Safety Analysis Report Section 6.3, Isolation Condenser System, Revision 18
: SE-328312-003,
: GL 89-10 Motor Operated Valve Modification, Revision 1
: SE-315403-031, Justification for Revised C Hi Flow Trip Time Delay, Revision 1
: Adverse Condition Monitoring and Contingency Plan for Increase in Unidentified Leak Rate, dated April 17, 2015
: 1-8 Sump Chemistry Sample, dated April 24, 2015
==Section 1EP6: Drill Evaluation==
===Procedures===
: EP-AA-112-100, Control Room Operations, Revision 13
: EP-AA-112-100-F-01, Shift Emergency Director Checklist, Revision U
: EP-AA-112-100-F-06, ERO Notification or Augmentation, Revision Q
: EP-AA-114-F-02, BWR Release In Progress Determination Guidance, Revision A
==Section 2RS5: Radiation Monitoring Instrumentation==
===Procedures===
: 621.3.005, High Radiation Monitor - Reactor Building, Isolation - Calibration, Revision 54
: 621.3.023, Stack RAGEMS Sample and Effluent Flow Calibrations, Revision 25
: 621.3.024, Stack RAGEMS Sample and Effluent Flow
: Functional Test, Revision 5 621.3.025, Stack RAGEMS Noble Gas Monitor Calibration, Revision 33
: 621.3.026, Stack RAGEMS Noble Gas Monitor Functional Test, Revision 32
: 621.3.034, Turbine Building RAGEMS Sample and Effluent Flow
: Calibration, Revision 15
: 621.3.036, Turbine Building RAGEMS Noble Gas Channel Calibration, Revision 12
: 621.3.037, Turbine Building RAGEMS Noble Gas Monitor
: Functional Test, Revision 27
: 621.3.038, Stack and Turbine Building RAGEMS High Range Monitor
: Calibration, Revision 15
: 621.3.041, Service Water Radiation Monitoring System Calibration (RN01A, M-3-001, RN08C, RN31B), Revision 16 621.3.043, Service Water Radiation Monitor Functional Test, Revision 10 621.3.045, Turbine Building RAGEMS Sample and Effluent Flow
: Functional Test, Revision 13 681.4.004, Technical Specification Log sheets for Daily Source Checks, Revision 30
===Documents===
: Oyster Creek System Health Report, 661
: Radiation Monitoring System, Q4-2014 Oyster Creek System Health Report, 661
: Radiation Monitoring System, Q1-2015 WO R2248776, Surveillance 621.3.005, High Radiation Monitor - RX. Building, Isolation
: Calibration, January 8, 2015 WO R2253509, Surveillance 621.3.005, High Radiation Monitor - RX. Building, Isolation
: Calibration, April 29, 2015 WO R2155453, Surveillance 621.3.025, Stack RAGEMS Noble Gas monitor Calibration, March 7, 2012 WO R2204250, Surveillance 621.3.025, Stack RAGEMS Noble Gas Monitor Calibration, April 26, 2014
: WO 2250803, Surveillance 621.3.026, Stack RAGEMS Noble Gas Monitor
: Functional Test, February 10, 2015
: WO 2254601, Surveillance 621.3.026, Stack RAGEMS Noble Gas Monitor
: Functional Test, May 12, 2015
===Condition Reports===
: 2458935
: 1632490
: 2486056
: 2466905
: 2464332
: 2453176
: 2434407
: 1628653
: 1620160
: 1613493 1603392
==Section 2RS6: Radioactive Gaseous and Liquid Effluent Treatment==
===Procedures===
: CY-OC-170-201, Compliance with Technical Specification 6.8.4 Radioactive Effluent Control, Revision 2
: CY-OC-170-3010, Cross Reference of Technical Specifications, ODCM Requirement and Compliance Requirements, Revision 3
: CY-AA-170-000, Radioactive Effluent and Environmental Monitoring Programs, Revision 6
: CY-AA-170-200, Radioactive Effluents Control Program, Revision 2
: CY-OC-170-302, Chemistry Surveillance Test Program, Revision 4
: CY-OC-120-900, Stack Effluent Sampling and Analysis, Revision 21
: CY-OC-120-910, Turbine Building Ventilation System Sampling, Revision 12
: CY-OC-120-920, AOG Building Effluent Sampling and Analysis, Revision 16
: CY-OC-120-921, AOG Building Process Gas and Water Sampling and Analysis, Revision 0
: CY-OC-170-2020, Radiological Abnormal Gaseous and Liquid Release Assessment, Revision 1
: CY-OC-170-3001, Stack Alternate Sampling, Revision 1
: CY-OC-120-9000, Monthly RAGEMS Particulate Filter Composite, Revision 7
: CY-AA-130-320, Packard 2900TR/3100TR Liquid Scintillation Counter, Revision 3
: CY-OC-130-530, Tritium Analysis Liquid Samples, Revision 8
: CY-AA-170-2000, Annual Radioactive Effluent Release Report, Revision 7
: CY-AA-170-210, Potentially Contaminated System Control Program, Revision 1
: RP-AA-303, Soil Sampling for Radiological Analysis, Revision 0
: EN-OC-402-100, NJPDES Sampling and Analysis, Revision 15 406.8, Operations of Stack RAGEMS, Revision 43 406.9, Operation of the Turbine Building RAGEMS, Revision 26 420, Instrumentation Setpoints, Revision 14
: EN-A-408-4000, Radiological Groundwater Protection Program Implementation, Revision 5
: EN-OC-408-4001, RGPP Onsite and Offsite Sample Results Comparison, Revision 0
: EN-OC-408-4160, RGPP Reference Material for Oyster Creek Generating Station, Revision 6
: CY-OC-120-706, Groundwater Remediation Process Sample Collection, Revision 5
: CY-AA-130-201, Radiochemistry Quality Control, Revision 3
: CY-AA-170-1100, Quality Assurance for Radiological Monitoring Programs, Revision 2
: CY-AA-170-2100, Estimated Errors of Effluent Measurements, Revision 1
: CY-OC-170-2001, Quality Control for Radioactive Effluents, Revision 1
: CY-AA-130-201-F-02, Regulatory Position for Regulatory Guide 4.15, Revision 1
===Documents===
: RA-13-055, Oyster Creek Nuclear Generating Station Annual Radioactive Effluent Release Report for 2013, April 30, 2014
: RA-14-002, Oyster Creek Nuclear Generating Station Annual Radioactive Effluent Release Report for 2014, April 30, 2015 Oyster Creek Offsite Dose Calculation Manual, Revision 6
: LS-AA-126-1005 Attachment 2 Check-In Self-assessment Report
: AR 1657492,
: ANI 07-01 Potential for Unmonitored and Unplanned Off-site Release of Radioactive Material, July 24, 2014 L020311.164, American Nuclear Insurers Liability Insurance Inspection, February 1
: 3, 2011 EPRI Groundwater Protection Program, Groundwater Protection Initiative Self-assessment
: Oyster Creek Nuclear Generating Station, October 2013 W.O. R2229067, Surveillance 651.1.003 Standby Gas Treatment System #1
: Charcoal Filter In-Place Leak Test, March 17, 2015 W.O. R2224329, Surveillance 651.3.103 Standby Gas Treatment System #2 In place Leak Test, July 30, 2014 W.O. R2226085, Surveillance 651.1.002 Standby Gas Treatment System #1Particulate Filter In-Place Leak Test, March 18, 2015 W.O. R2221718 Surveillance 651.3.102 Standby Gas Treatment System #2
: Particulate Filter In-Place Leak Test, May 6, 2014 NUCON International Lab ID W429, OCGS Sample Charcoal F-28-3 SGTS #1, April 1, 2015 NUCON International Lab ID W509, OCGS Sample Charcoal 1690-09 SGTS #2, May 6, 2015 WO R2147672, Surveillance 621.3.034 Turbine Building RAGEMS Sample and Effluent Flow -Calibration, February 18, 2011 WO R2231218, Surveillance 621.3.034 Turbine Building RAGEMS Sample and Effluent Flow -Calibration, November 12, 2014
: WO2251965, Surveillance 621.3.045 Turbine Building RAGEMS Sample and Effluent Flow-Functional Test, February 11, 2015
: WO2254898, Surveillance 621.3.045 Turbine Building RAGEMS Sample and Effluent Flow-Functional Test, May 18, 2015 WO R2211228, Surveillance 621.3.023 Stack RAGEMS Sample and Effluent Flow Calibration, November 6, 2013 WO R2234210, Surveillance 621.3.023 Stack RAGEMS Sample and Effluent Flow Calibration, December 18, 2014 Calculation No.
: OCGS-007, Service Water Radiation Monitor Setpoints, April 13, 2011 Radiation Protection Calculation and Position Paper
: OC-14-002, 2013
: 2014 10CFR61 Waste Stream Analysis, February 6, 2014 Conestoga Rovers Associates, Hydrological Investigation Report - Revision 2, April 2011 Conestoga Rovers Associates, Oyster Creek Monitoring Well Inspection, May 13, 2015 Normandeau, Groundwater Well Inspection/Maintenance Log, April 13, 2015 Normandeau, Groundwater Well Inspection/Maintenance Log, January 12, 2015 Tech Eval
: 01617346-30 Oyster Creek Engineering Evaluation of Buried Piping Inspections for Reasonable Assurance, October 23, 2014 UCC Report No.
: RCN-005 Condensate Storage Tank Underwater Cleaning and
: VT-3 Inspection, May 2009 
: SRRS 2B.135, Oyster Creek List Required by
: RP-AA-228 for 10
: CFR 50.75(g) Decommissioning Records, March 26, 2015 SRRS 5C.101, Oyster Creek Buried Pipe Mitigation Project 10
: CFR 50.75(g)2. Record, April 14, 2014 Eckert & Ziegler Analytical Results of Radiochemistry Cross Check Program EXELON Oyster Creek 3rd Quarter October 7, 2014 Teledyne Brown Engineering Environmental Services 2014 Quality Assurance Report, December 22, 2014
: Normandeau Associates, Inc. letter from Dennis Fillman to Mathew Nixon RE: 2013 Land Use Census Report Oyster Creek Generating Station, August 2013
===Condition Reports===
: 2501639
: 2431211
: 2411074
: 1548306
: 1547234 1500072
==Section 4OA1: Performance Indicator Verification==
===Procedures===
: ABN-1, Reactor Scram, Revision 11
===Condition Reports===
: 2500776
===Miscellaneous===
: NUREG 1022, Reporting Requirements, Revision 3
: Various Operator Logs from April 1, 2014 to March 31, 2015
: NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7
==Section 4OA2: Problem Identification and Resolution==
===Procedures===
: PI-AA-120, Issue Identification and Screening Process, Revision 1
: PI-AA-125, Corrective Action Program (CAP) Procedure, Revision 2
: WC-AA-106, Work Screening and Processing, Revision 15
==Section 4OA3: Follow-up of Events and Notices of Enforcement Discretion==


===Procedures===
: 201, Plant Startup, Revision 101 303, Reactor Cleanup Demineralizer System, Revision 144 421, EX2100e HMI, Trouble and Fault Alarms, Revision 4
: MA-AA-716-010, Maintenance Planning, Revision 22
: MA-AA-716-235, Control of Critical Digital Asset (CDA) Portable Media and Portable Devices, Revision 3
: MA-AA-716-012, Post Maintenance Testing, Revision 20
: MA-MA-716-010-1005, Work Order (W/O) Planning Process, Revision 18
: MA-MA-716-010-1008, Work Order (W/O) Work Performance, Revision 5
: MA-AA-716-003, Tool Pouch/Minor Maintenance, Revision 8
: HU-AA-1211, Pre-job Briefings, Revision 10
: HU-AA-101, Human Performance Tools and Verification Practices, Revision 9
: HU-AA-104-101, Procedure Use and Adherence, Revision 5
: WC-AA-104, Integrated Risk Management, Revision 23
===Condition Reports===
: 2394374
: 2394357
: 2402030
: 2504265
: 2474619
===Drawings===
: GE 148F444, Clean Up Demineralizer System, Revision 104
: Maintenance Orders/Work Orders A2362493
==LIST OF ACRONYMS==
: [[AC]] [[alternating current]]
: [[ADAMS]] [[Agencywide Documents Access and Management System]]
: [[AVR]] [[automatic voltage regulator]]
: [[CFR]] [[Code of Federal Regulations CO2  carbon dioxide]]
: [[FIN]] [[Finding]]
: [[GPI]] [[groundwater protection initiative]]
: [[HMI]] [[human machine interface]]
: [[IMC]] [[Inspection Manual Chapter]]
: [[IST]] [[in-service test kV  kilovolt]]
: [[LER]] [[Licensee Event Report]]
: [[NCV]] [[non-cited violation]]
: [[NEI]] [[Nuclear Energy Institute]]
: [[NRC]] [[Nuclear Regulatory Commission]]
: [[ODCM]] [[Offsite Dose Calculation Manual]]
: [[PCV]] [[pressure control valve]]
: [[RCS]] [[reactor coolant system]]
: [[RWCU]] [[reactor water cleanup]]
: [[SDP]] [[significance determination process]]
: [[SSC]] [[structure, system, or component]]
: [[UFSAR]] [[Updated Final Safety Analysis Report]]
}}
}}

Latest revision as of 09:34, 10 January 2025

IR 05000219/2015002, April 1, 2015 - June 30, 2015, Oyster Creek Nuclear Generating Station, Integrated Inspection Report
ML15224B475
Person / Time
Site: Oyster Creek
Issue date: 08/12/2015
From: Silas Kennedy
NRC/RGN-I/DRP/PB6
To: Bryan Hanson
Exelon Generation Co, Exelon Nuclear
KENNEDY, SR
References
IR 2015002
Download: ML15224B475 (43)


Text

August 12, 2015

SUBJECT:

OYSTER CREEK NUCLEAR GENERATING STATION - INTEGRATED INSPECTION REPORT 05000219/2015002

Dear Mr. Hanson:

On June 30, 2015, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Oyster Creek Nuclear Generating Station. The enclosed inspection report documents the inspection results, which were discussed on July 10, 2015, with Mr. G. Stathes, Site Vice President, and other members of your staff.

NRC inspectors examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

The inspectors documented four findings of very low safety significance (Green) in this report.

One finding involved a violation of NRC requirements. Because of the very low safety significance, and because they are entered into your corrective action program, the NRC is treating these findings as non-cited violations, consistent with Section 2.3.2.a of the NRC Enforcement Policy.

If you contest the non-cited violations in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at Oyster Creek Nuclear Generating Station. In addition, if you disagree with the cross-cutting aspect assigned to any finding, or a finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region I, and the NRC Resident Inspector at Oyster Creek Nuclear Generating Station. In accordance with Title 10 of the Code of Federal Regulations (CFR) 2.390 of the NRCs Rules of Practice, a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRCs Public Document Room or from the Publicly Available Records component of the NRCs Agencywide Documents Access Management System (ADAMS). ADAMS is accessible from the NRC website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Silas R. Kennedy, Chief Reactor Projects Branch 6 Division of Reactor Projects

Docket Nos. 50-219 License Nos. DPR-16

Enclosure:

Inspection Report 05000219/2015002 w/Attachment: Supplementary Information

REGION I==

Docket Nos.:

50-219

License Nos.:

DPR-16

Report No.:

05000219/2015002

Licensee:

Exelon Nuclear

Facility:

Oyster Creek Nuclear Generating Station

Location:

Forked River, New Jersey

Dates:

April 1, 2015 - June 30, 2015

Inspectors:

A. Patel, Senior Resident Inspector E. Andrews, Resident Inspector B. Dionne, Health Physicist S. Elkhiamy, Project Engineer T. Fish, Senior Operations Examiner M. Patel, Operations Examiner

Approved By:

Silas R. Kennedy, Chief

Reactor Projects Branch 6

Division of Reactor Projects

SUMMARY OF FINDINGS

IR 05000219/2015002; 04/01/2015 - 06/30/2015; Exelon Energy Company, LLC, Oyster Creek

Generating Station; Internal Flooding, Licensed Operator Requalification Program, Follow-Up of Events.

This report covered a three-month period of inspection by resident inspectors and announced inspections performed by regional inspectors. One NRC-identified finding and two self-revealing findings of very low safety significance (Green) were identified during this inspection.

Additionally, a self-revealing non-cited violation (NCV) of very low safety significance (Green)was also documented in this report. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP), dated April 29, 2015. The cross-cutting aspects for the findings were determined using IMC 0310, Aspects Within Cross-Cutting Areas, dated December 4, 2014. All violations of NRC requirements are dispositioned in accordance with the NRCs Enforcement Policy, dated February 4, 2015. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 5.

Cornerstone: Initiating Events

Green.

A self-revealing NCV of Technical Specification 6.8.1(a), Procedures and Programs, was identified because Exelon did not follow procedure 303, Reactor Cleanup Demineralizer System, during the system restoration on March 26, 2015. Specifically, during startup from a forced outage (1F36), Exelon did not follow procedure 303, which required correct valve lineups for system restoration of reactor water cleanup (RWCU) after system isolation. This resulted in decreasing reactor water level, which was automatically terminated by a second RWCU isolation. Exelon entered this issue into the corrective action program. Planned corrective actions include enhancing operator training in system knowledge and procedure compliance and revising startup procedures.

This finding is determined to be more than minor because it is associated with the human performance attribute of the Initiating Events cornerstone and affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, Exelon did not properly lineup the RWCU system after isolation, which resulted in a water level transient and challenging the critical safety function of inventory control. This finding is determined to be of very low safety significance (Green), because it did not cause a reactor trip and the loss of mitigation equipment relied upon to transition the plant from the onset of the trip to a stable shutdown condition. This finding has a cross-cutting aspect in the area of Human Performance, Challenge the Unknown, because Exelon did not recognize and plan for the possibility of mistakes, or implement appropriate error reduction tools. Specifically, the operators did not stop and fully communicate plant condition after the initial RWCU isolation.

Consequently, operators opened the RWCU system inlet valve due to the increasing water level without following procedure guidance. [H.11] (Section 4OA3)

Green.

A self-revealing finding was identified because Exelon did not properly screen work in accordance with MA-AA-716-010, Maintenance Planning. Specifically, on September 12, 2014, Exelon did not screen the automatic voltage regulators (AVR) human machine interface (HMI) post-maintenance test per the maintenance planning procedure.

As a result, on October 12, 2014, Exelon personnel performing the post-maintenance test did not have a work order, which would have included plant configurations and limitations associated with the test. This led to an automatic reactor scram. Exelon entered this issue into the corrective action program. Planned corrective actions include reinforcing with work planners that a work order is required for similar work activities.

This finding was determined to be more than minor because it is associated with the human performance attribute of the Initiating Events cornerstone and affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during plant operation. Specifically, resetting the three AVR controllers caused an automatic plant scram. This finding is determined to be of very low safety significance (Green), because it did not cause a reactor trip and the loss of mitigation equipment relied upon to transition the plant from the onset of the trip to a stable shutdown condition. This finding has a cross-cutting aspect in the area of Human Performance, Challenge the Unknown, because Exelon did not recognize and plan for the possibility of mistakes, or implement appropriate error reduction tools. Specifically, on October 12, 2014, Exelon personnel did not stop when faced with the uncertain situation of the HMI screen that did not respond as expected. [H.11] (Section 4OA3)

Cornerstone: Mitigating Systems

Green.

The inspectors identified a finding associated with Exelon procedure, OP-AA-108-115, Operability Determinations, because Exelon did not adequately assess a degraded floor gasket for the D emergency 4 kilovolt (kV) switchgear roll-up door. Specifically,

Exelon did not adequately assess the flood and fire functionality of the degraded gasket, which is credited to provide protection to safety-related D emergency 4kV switchgear during a postulated internal flood event and to contain the carbon dioxide (CO2) gaseous suppression system during a postulated fire within the D switchgear room. Exelon entered this issue into the corrective action program. Planned corrective actions include reinforcing the operability determination procedure and enhancing operator training in fire and flood functionality of gaskets. Additional corrective actions included repairing the gasket and performing a detailed analysis of the ability of degraded gasket to meet its flooding and fire function.

This finding is more than minor because it is associated with the protection against external factors attribute of the Mitigating Systems cornerstone, and affected the cornerstone objective of ensuring the reliability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the degraded floor gasket could have resulted in increased water level in the D emergency 4kV switchgear room during a postulated internal flood due to a fire water pipe rupture, therefore affecting the reliability of the D emergency 4k switchgear to perform its safety function. In addition, the degraded floor gasket could have resulted in CO2 leakage out of the D emergency 4k switchgear room during a postulated fire in that room, therefore affecting the reliability of the D emergency 4k switchgear gaseous suppression system to perform its safety function. The inspectors determined that this finding is of very low safety significance (Green) because it is a deficiency that affected the design or qualification of a mitigating structure, system, or component (SSC), where the SSC maintained its operability or functionality. This finding has a cross-cutting aspect in the area of Problem Identification and Resolution, Evaluation, because Exelon did not thoroughly evaluate issues to ensure that resolutions address the causes and extent of conditions commensurate with their safety significance. Specifically,

Exelon staff did not thoroughly evaluate the issue associated with the degraded floor gasket for fire and flood functionality. [P.2] (Section 1R06)

Green.

A self-revealing finding was identified associated with inadequate licensed operator performance during licensed operator requalification exams in accordance with TQ-AA-150,

Operator Training Program. Specifically, two of seven crews failed the simulator scenario portion of the requalification examinations. As an immediate corrective action, the crews that failed were restricted from licensed duties. Exelon entered this issue into the corrective action program, and facility training staff remediated the crews (the crews were retrained and successfully retested), and those crews were returned to licensed duties.

This finding is more than minor because it is associated with the human performance attribute of the Mitigating Systems cornerstone and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, two of seven crews failed to demonstrate a satisfactory understanding of the knowledge and abilities required to safely operate the facility under normal, abnormal, and emergency conditions. The inspectors determined the finding to be of very low safety significance (Green) because it is related to requalification exam results, did not result in a failure rate of greater than forty percent, and the two crews were remediated (i.e., the crews were retrained and successfully retested)prior to returning to shift. This finding has a cross-cutting aspect in the area of Human Performance, Training, because Exelon staff did not provide adequate operator requalification training to maintain a knowledgeable, technically competent workforce. [H.9]

(Section 1R11)

REPORT DETAILS

Summary of Plant Status

Oyster Creek began the inspection period at 100 percent power. On May 7, 2015, an automatic reactor scram occurred due to a turbine trip caused by a failure of the main transformer digital protection relay system. After repairs to the digital protection relay system, operators commenced plant startup on May 12 and returned to full power operation on May

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection

.1 Readiness for Seasonal Extreme Weather Conditions

a. Inspection Scope

The inspectors performed a review of Exelons readiness for the onset of seasonal high temperatures. The review focused on the emergency service water and the emergency diesel generators. The inspectors reviewed the Updated Final Safety Analysis Report (UFSAR), technical specifications, control room logs, and the corrective action program to determine what temperatures or other seasonal weather could challenge these systems, and to ensure Exelon personnel had adequately prepared for these challenges.

The inspectors reviewed station procedures, including Exelons seasonal weather preparation procedure and applicable operating procedures. The inspectors performed walkdowns of the selected systems to ensure station personnel identified issues that could challenge the operability of the systems during hot weather conditions.

Documents reviewed for each section of this inspection report are listed in the

.

b. Findings

No findings were identified.

.2 Summer Readiness of Offsite and Alternate Alternating Current (AC) Power Systems

a. Inspection Scope

The inspectors performed a review of plant features and procedures for the operation and continued availability of the offsite and alternate AC power system to evaluate readiness of the systems prior to seasonal high grid loading. The inspectors reviewed Exelons procedures affecting these areas and the communications protocols between the transmission system operator and Exelon. This review focused on changes to the established program and material condition of the offsite and alternate AC power equipment. The inspectors assessed whether Exelon established and implemented appropriate procedures and protocols to monitor and maintain availability and reliability of both the offsite AC power system and the onsite alternate AC power system. The inspectors evaluated the material condition of the associated equipment by interviewing the responsible system manager, reviewing condition reports and open work orders, and walking down portions of the offsite and AC power.

b. Findings

No findings were identified.

==1R04 Equipment Alignment

==

.1 Partial System Walkdowns

a. Inspection Scope

The inspectors performed partial walkdowns of the following systems:

Standby liquid control system on April 2, 2015

A, B, and C emergency service water pumps while D emergency service water pump out of service on April 21, 2015

Turbine building closed cooling water system on April 28, 2015

A and B isolation condensers prior to startup from the forced outage (1F37) on May 12, 2015

No. 1 emergency diesel generator while No. 2 emergency diesel generator out of service on May 18, 2015

The inspectors selected these systems based on their risk-significance relative to the reactor safety cornerstones at the time they were inspected. The inspectors reviewed applicable operating procedures, system diagrams, the UFSAR, technical specifications, work orders, condition reports, and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have impacted the systems performance of its intended safety functions. The inspectors also performed field walkdowns of accessible portions of the systems to verify system components and support equipment were aligned correctly and were operable. The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no deficiencies. The inspectors also reviewed whether Exelon staff had properly identified equipment issues and entered them into the corrective action program for resolution with the appropriate significance characterization.

b. Findings

No findings were identified.

==1R05 Fire Protection

==

.1 Resident Inspector Quarterly Walkdowns

a. Inspection Scope

The inspectors conducted tours of the areas listed below to assess the material condition and operational status of fire protection features. The inspectors verified that Exelon personnel controlled combustible materials and ignition sources in accordance with administrative procedures. The inspectors verified that fire protection and suppression equipment was available for use as specified in the area pre-fire plan, and passive fire barriers were maintained in good material condition. The inspectors also verified that station personnel implemented compensatory measures for out of service, degraded, or inoperable fire protection equipment, as applicable, in accordance with procedures.

Lower cable spreading room on April 8, 2015

Turbine building basement south on April 8, 2015

Feed pump room on April 8, 2015

Emergency diesel generator room No. 2 on April 15, 2015

Reactor building southeast corner room on April 15, 2015

Reactor building equipment drain tank room on May 19, 2015

b. Findings

No findings were identified.

1R06 Flood Protection Measures

.1 Internal Flooding Review

a. Inspection Scope

The inspectors reviewed the UFSAR, the site flooding analysis, and plant procedures to assess susceptibilities involving internal flooding. The inspectors also reviewed the corrective action program to determine if Exelon identified and corrected flooding problems and whether operator actions for coping with flooding were adequate. The inspectors focused on the reactor building southeast corner room area and turbine building switchgear area to verify the adequacy of equipment seals located below the flood line, floor and water penetration seals, watertight door seals, common drain lines and sumps, sump pumps, level alarms, control circuits, and temporary or removable flood barriers.

b. Findings

Introduction.

The inspectors identified a Green finding associated with Exelon procedure, OP-AA-108-115, Operability Determinations, because Exelon did not adequately assess a degraded floor gasket for the D emergency 4kV switchgear roll-up door. Specifically, Exelon did not adequately assess the flood and fire functionality of the degraded gasket, which is credited to provide protection to the safety-related D emergency 4kV switchgear during a postulated internal flood event and to contain the CO2 gaseous suppression system during a postulated fire within the D switchgear room.

Description.

During a system walk down on May 29, 2015, NRC inspectors identified a degraded floor gasket for the D emergency 4kV switchgear roll-up door and informed Operations. Operations wrote issue report 2507389 to evaluate the degraded floor gasket flood functionality. The inspectors noted that the degraded floor gasket could result in increased water level in the D emergency 4kV switchgear room during a postulated internal flood event due to a fire water pipe rupture. Specifically, OC-PSA-12, Internal Flood Evaluation Summary Notebook, states, in part, The rollup doors have gaskets along the bottom edge that are assumed to preclude water propagation.

The inspectors additionally identified that Operations did not consider the impact on the CO2 system and, as a result, did not establish a continuous fire watch with backup fire suppression equipment as stated in Exelon procedure 101.2, Oyster Creek Site Fire Protection Program. Exelon procedure 101.2, states, in part, an inoperable fire barrier (penetration seals, dampers, doors, breaches in walls/floors/ceilings) could render a gaseous fire suppression system inoperable. In this event, the actions for an inoperable CO2 system and the actions for an inoperable fire rated assembly must be completed.

With the CO2 system inoperable, within one hour, establish a continuous fire watch with backup fire suppression equipment.

The inspectors noted that Exelon personnel originally identified the degraded floor gasket in December 2014 and documented this issue in issue report 2423574. The inspector reviewed the issue report and noted that Operations did not adequately evaluate the degraded barrier for flooding and fire functionality. The issue report stated that the gasket did not affect the doors integrity or ability to act as a fire door. Also, the issue report did not address the degraded gaskets affect during internal flooding events.

The inspectors also reviewed issue report 2423574 to ascertain the corrective actions for the degraded floor gasket. The actions specified Exelon personnel to complete repairs to the floor gasket in work order R2249794. The actions in this work order were stated as complete, although the inspectors identified on May 29, 2015, the degraded floor gasket was not repaired.

The inspectors concluded that the degraded floor gasket was not properly assessed for fire or flooding functionality when Operations first identified the issue in December 2014 (issue report 2423574) and for fire functionality when the inspectors bought this issue to Operations attention on May 29, 2015. The inspectors determined that this is contrary to the requirements of OP-AA-108-115, Operability Determinations. This procedure states in part, Structures may be required to be operable by the Technical Specifications, or they may be related to support functions for system, structure and component (SSC) in the TS. Examples of structural degradation are degradation of door and penetration sealing. If a structure is degraded, the structures capability of performing its specified function should be assessed. Also, Exelon procedure OP-AA-108-115-1002, Supplemental Consideration for On-Shift Immediate Operability Determinations, states, in part, the ability of a SSC to meet regulatory requirements, codes, industry standards, (e.g., Fire Protection analysis, Appendix R, Safe Shutdown capability) or non-conformances affecting internal flooding concerns are thoroughly assessed.

Immediate corrective actions, following identification by the inspectors, included placing a sandbag in the area of the degraded gasket. As additional corrective actions, Exelon conducted a detailed analysis of the degraded gasket to determine if the flooding and fire functions were affected. Exelon determined that the increase of water level in the D switchgear room due to the degraded gasket was below the level that would impact the D switchgear during the postulated fire water pipe break. Exelon determined that the CO2 system could compensate for leakage through the degraded gasket and would still be capable of extinguishing a postulated fire within the D switchgear room. Also, corrective actions included reinforcing the operability determination procedure, enhancing operator training in fire and flood functionality of gaskets, and repairing the gasket.

Analysis.

The inspectors determined that inadequate assessment for fire or flooding functionality of the D switchgear roll-up door degraded floor gasket, in accordance with OP-AA-108-115, is a performance deficiency that was within Exelons ability to foresee and correct. The finding is more than minor because it is associated with the protection against external factors attribute of the Mitigating Systems cornerstone and affected the cornerstone objective to ensure the reliability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the degraded floor gasket could have resulted in increased water level in the D emergency 4k switchgear room during a postulated internal flood due to a fire water pipe rupture, therefore affecting the reliability of the D emergency 4k switchgear to perform its safety function. In addition, the degraded floor gasket could have resulted in CO2 leakage out of the D emergency 4k switchgear room during a postulated fire in that room, therefore affecting the reliability of the D emergency 4k switchgear gaseous suppression system to perform its safety function.

The inspectors evaluated the finding using 0609.04, Initial Characterization of Findings, and IMC 0609, Appendix A, Exhibit 2, Mitigating System Screening Questions. The inspectors determined that this finding is a deficiency that affected the design or qualification of a mitigating SSC, where the SSC maintained its operability or functionality. Therefore, inspectors determined the finding to be of very low safety significance (Green).

This finding has a cross-cutting aspect in the area of Problem Identification and Resolution, Evaluation, because Exelon did not thoroughly evaluate issues to ensure that resolutions address the causes and extent of conditions commensurate with their safety significance. Specifically, Exelon staff did not thoroughly evaluate the issue associated with the degraded floor gasket for fire and flood functionality. [P.2]

Enforcement.

This finding does not involve enforcement action because no violation of regulatory requirements was identified. Exelon entered this issue into their corrective action program as issue report 2507389. Because this issue did not involve a violation and has very low safety significance, it is identified as a finding. (FIN

===05000219/2015002-01, Inadequate Assessment of 4kV Emergency Switchgear Roll-Up Door Degraded Floor Gasket).

.2 Annual Review of Cables Located in Underground Bunkers/Manholes

a. Inspection Scope

The inspectors conducted an inspection of underground bunkers/manholes subject to flooding that contain cables whose failure could disable risk-significant equipment.

The inspectors performed walkdowns of risk-significant areas, including the SBO3 (MH-743-3), containing 13.8kV cables from the combusting turbine, and the intake area manhole (MH-731-1), containing 4160V cables from the emergency service water pumps, to verify that the cables were not submerged in water, that cables and/or splices appeared intact, and to observe the condition of cable support structures. When applicable, the inspectors verified proper sump pump operation and verified level alarm circuits were set in accordance with station procedures and calculations to ensure that the cables will not be submerged. The inspectors also ensured that drainage was provided and functioning properly in areas where dewatering devices were not installed.

b. Findings

No findings were identified.

==1R07 Heat Sink Performance (711111.07A - 1 sample)

a. Inspection Scope

==

The inspectors reviewed the 1-1 reactor building closed cooling water heat exchanger to determine its readiness and availability to perform its safety functions. The inspectors reviewed the design basis for the component and verified Exelons commitments to NRC Generic Letter 89-13. The inspectors reviewed the cleaning and inspection of the heat exchanger, discussed the results of the most recent inspection with engineering staff, and reviewed pictures of the as-found and as-left conditions. The inspectors verified that Exelon initiated appropriate corrective actions for identified deficiencies. The inspectors also verified that the number of tubes plugged within the heat exchanger did not exceed the maximum amount allowed.

b. Findings

No findings were identified.

==1R11 Licensed Operator Requalification Program

==

.1 Quarterly Review of Licensed Operator Requalification Testing and Training

(71111.11Q - 1 sample)

a. Inspection Scope

The inspectors observed licensed operator simulator training on April 14, 2015, which included a control rod drive pump trip, hydraulic anticipated transient without scram, and isolation condenser steam leak. The inspectors evaluated operator performance during the simulated event and verified completion of risk significant operator actions, including the use of abnormal and emergency operating procedures. The inspectors assessed the clarity and effectiveness of communications, implementation of actions in response to alarms and degrading plant conditions, and the oversight and direction provided by the control room supervisor. The inspectors verified the accuracy and timeliness of the emergency classification made by the shift manager and the technical specification action statements entered by the shift technical advisor. Additionally, the inspectors assessed the ability of the crew and training staff to identify and document crew performance problems.

b. Findings

No findings were identified.

.2 Quarterly Review of Licensed Operator Performance in the Main Control Room

(71111.11Q - 1 sample)

a. Inspection Scope

The inspectors observed control room operator performance as they entered cold shutdown to start a forced outage (1F37) on May 8, 2015. The inspectors observed infrequently performed test or evolution briefings, shift turnover briefings, and alarm response. Additionally, the inspectors observed control room operator performance to verify that procedure use, crew communications, and coordination of activities between work groups similarly met established expectations and standards.

b. Findings

No findings were identified.

.3 Licensed Operator Requalification

a. Inspection Scope

The following inspection activities were performed using NUREG-1021, "Operator Licensing Examination Standards for Power Reactors," Revision 9, Supplement 1, and Inspection Procedure Attachment 71111.11, Licensed Operator Requalification Program. The inspection assessed whether pass rates were consistent with the guidance of NRC Manual Chapter 0609, Appendix I, and Operator Requalification Human Performance Significance Determination Process (SDP).

Examination Results

On July 1, 2015, the results of the comprehensive written and annual operating tests were reviewed to determine if pass/fail rates were consistent with the guidance of NUREG-1021, Revision 9, Supplement 1 and NRC IMC 0609, Appendix I, Operator Requalification Human Performance Significance Determination Process (SDP). The review determined that the individual operator failure rate was less than 20 percent, however, the crew failure rate exceeded 20 percent.

b. Findings

Introduction:

A self-revealing Green finding was identified associated with inadequate licensed operator performance during licensed operator requalification exams in accordance with TQ-AA-150, Operator Training Program. Specifically, two of seven crews failed the simulator scenario portion of the requalification examinations.

Description:

During the week of June 8, 2015, Exelons training staff administered requalification examinations to licensed operators. Exelon staff evaluated crew performance during dynamic simulator scenarios and individual operator performance during job performance measures and on the written examination. Exelon evaluation of the requalification examination showed that two of seven crews (which represents a failure rate of 28.6 percent) failed the simulator scenario portion of the examination. This failure rate exceeded the threshold failure rate of 20 percent as specified in TQ-AA-150, Operator Training Program. Specifically, Attachment F25, LORT Annual Exam Status Report states, in part, that simulator crew failure rate greater than 20 percent but less than 40 percent constitutes as a Green finding.

Exelon initiated issue report 2513013 to address the high failure rate on the annual requalification examinations, restricted the failed crews from licensed duties, conducted crew and individual operator remediation, and began conducting a root cause evaluation to develop long-term corrective actions.

Analysis:

The inspectors determined that the crew failure rate of greater than 20 percent, as specified in TQ-AA-150, is a performance deficiency that was reasonably within Exelons ability to foresee and correct. This finding is more than minor because it is associated with the Mitigating Systems cornerstone attribute of human performance and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, two of seven crews failed to demonstrate a satisfactory understanding of the knowledge and abilities required to safely operate the facility under normal, abnormal, and emergency conditions. Licensed operators are expected to operate the plant within acceptable standards of knowledge and abilities demonstrated through periodic testing. The inspectors evaluated this performance deficiency using Inspection Manual Chapter 0609.04, "Initial Characterization of Findings," Appendix I, "Licensed Operator Requalification Significance Determination Process." This finding is of very low safety significance (Green) because the finding is related to requalification exam results, did not result in a failure rate of greater than 40 percent, and the two crews were remediated (i.e., the licensed operators were retrained and successfully retested)prior to returning to shift.

This finding has a cross-cutting aspect in the area of Human Performance, Training, because Exelon did not initially provide adequate operator requalification training to maintain a knowledgeable, technically competent workforce. [H.9]

Enforcement:

This finding does not involve enforcement action because no violation of regulatory requirements was identified. Exelon entered this issue into their corrective action program as issue report 2513013. Because this issue did not involve a violation and has very low safety significance (Green), it is identified as a finding.

(FIN 05000219/2015002-02, Failure Rates Exceed Twenty Percent for Annual Requalification Exam).

1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors reviewed the samples listed below to assess the effectiveness of maintenance activities on SSC performance and reliability. The inspectors reviewed system health reports, corrective action program documents, maintenance work orders, and maintenance rule basis documents to ensure that Exelon was identifying and properly evaluating performance problems within the scope of the maintenance rule.

For each sample selected, the inspectors verified that the SSC was properly scoped into the maintenance rule in accordance with 10 CFR 50.65 and verified that the (a)(2)performance criteria established by Exelon staff was reasonable. As applicable, for a SSC classified as (a)(1), the inspectors assessed the adequacy of goals and corrective actions to return the SSC to (a)(2). Additionally, the inspectors ensured that Exelon staff was identifying and addressing common cause failures that occurred within and across maintenance rule system boundaries.

Core spray system on June 2, 2015

Main transformers digital protection relay system on May 20, 2015

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed station evaluation and management of plant risk for the maintenance and emergent work activities listed below to verify that Exelon performed the appropriate risk assessments prior to removing equipment for work. The inspectors selected these activities based on potential risk significance relative to the reactor safety cornerstones. As applicable for each activity, the inspectors verified that Exelon personnel performed risk assessments as required by 10 CFR 50.65(a)(4) and that the assessments were accurate and complete. When Exelon performed emergent work, the inspectors verified that operations personnel promptly assessed and managed plant risk. The inspectors reviewed the scope of maintenance work and discussed the results of the assessment with Exelons risk analyst to verify plant conditions were consistent with the risk assessment. The inspectors also reviewed the technical specification requirements and inspected portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met.

A isolation condenser out of service for planned maintenance on April 1, 2015

B reactor building closed loop cooling water pump out for planned maintenance on April 21, 2015

1-2 service water pump out of service for planned maintenance on May 4, 2015

Forced outage yellow shutdown risk due to decay heat removal on May 8, 2015

No. 2 emergency diesel generator out of service for planned maintenance on May 18, 2015

b. Findings

No findings were identified.

1R15 Operability Determinations and Functionality Assessments

a. Inspection Scope

The inspectors reviewed operability determinations for the following degraded or non-conforming conditions:

Standby liquid control accumulator (Y-19-101) at 0 psig on April 1, 2015

Core spray booster pump (NZ03A) due to high differential pressure on June 2, 2015

Spent fuel pool boraflex fuel racks on June 3, 2015

Containment spray 51A breaker loose arc chutes on June 19, 2015

Emergency service water system I while spectacle flange in orifice position on June 22, 2015

Electromatic relief valve cutout switch part 21 on June 23, 2015

The inspectors selected these issues based on the risk significance of the associated components and systems. The inspectors evaluated the technical adequacy of the operability determinations to assess whether technical specification operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the technical specifications and UFSAR to Exelons evaluations to determine whether the components or systems were operable.

The inspectors determined, where appropriate, compliance with bounding limitations associated with the evaluations. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled by Exelon.

b. Findings

No findings were identified.

1R18 Plant Modifications

.1 Temporary Modifications

a. Inspection Scope

The inspectors reviewed the temporary modifications listed below to determine whether the modifications affected the safety functions of systems that are important to safety.

The inspectors reviewed 10 CFR 50.59 documentation and post-modification testing results, and conducted field walkdowns of the modifications to verify that the temporary modifications did not degrade the design bases, licensing bases, and performance capability of the affected systems.

Temporary configuration change TCC-1504-532-RO-22 - Emergency service water system I to service water cross connect by rotating a spectacle flange on May 29, 2015

b. Findings

No findings were identified.

.2 Permanent Modifications

a. Inspection Scope

The inspectors evaluated a modification to the automatic scram contactors surveillance test frequency by surveillance test interval evaluation form OC-15-01, Automatic SCRAM Contactor Surveillance Extension. The inspectors also evaluated a modification to the main transformer digital protection relay system by engineering change request 15-00197, ECR to Remove the Output Trip Functions from the Digital Protection Relay System. The inspectors verified that the design bases, licensing bases, and performance capability of the affected systems were not degraded by the modification. In addition, the inspectors reviewed modification documents associated with the upgrade and design changes. The inspectors also reviewed revisions to the control room alarm response procedures and interviewed engineering and operations personnel to ensure the procedure could be reasonably performed.

b. Findings

No findings were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed the post-maintenance tests for the maintenance activities listed below to verify that procedures and test activities adequately tested the safety functions that may have been affected by the maintenance activity, that the acceptance criteria in the procedure was consistent with the information in the applicable licensing basis and/or design basis documents, and that the test results were properly reviewed and accepted and problems were appropriately documented. The inspectors also walked down the affected job site, observed the pre-job brief and post-job critique where possible, confirmed work site cleanliness was maintained, and witnessed the test or reviewed test data to verify quality control hold point were performed and checked, and that results adequately demonstrated restoration of the affected safety functions.

Hydraulic control unit 46-39 following cooling water check valve (V-305-138)replacement on April 6, 2015

D emergency service water pump following D emergency service water pump motor replacement on April 22, 2015

Main transformers after sudden pressure relay addition on May 18, 2015

Emergency diesel generator No. 2 following battery replacement on May 19, 2015

b. Findings

No findings were identified.

1R20 Refueling and Other Outage Activities

a. Inspection Scope

The inspectors reviewed the stations work schedule and outage risk plan for Oyster Creek forced outage (1F37), which was conducted May 7 through May 14, 2015. The inspectors reviewed Exelons development and implementation of outage plans and schedules to verify that risk, industry experience, previous site-specific problems, and defense-in-depth were considered. During the outage, the inspectors observed portions of the shutdown and cooldown processes and monitored controls associated with the following outage activities:

Configuration management, including maintenance of defense-in-depth, commensurate with the outage plan for the key safety functions and compliance with the applicable technical specifications when taking equipment out of service

Implementation of clearance activities and confirmation that tags were properly hung and that equipment was appropriately configured to safely support the associated work or testing

Installation and configuration of reactor coolant pressure, level, and temperature instruments to provide accurate indication and instrument error accounting

Status and configuration of electrical systems and switchyard activities to ensure that technical specifications were met

Monitoring of decay heat removal operations

Impact of outage work on the ability of the operators to operate the spent fuel pool cooling system

Reactor water inventory controls, including flow paths, configurations, alternative means for inventory additions, and controls to prevent inventory loss

Activities that could affect reactivity

Maintenance of secondary containment as required by technical specifications

Fatigue management

Identification and resolution of problems related to refueling outage activities

b. Findings

No findings were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors observed performance of surveillance tests and/or reviewed test data of selected risk-significant SSCs to assess whether test results satisfied technical specifications, the UFSAR, and Exelon procedure requirements. The inspectors verified that test acceptance criteria were clear, tests demonstrated operational readiness and were consistent with design documentation, test instrumentation had current calibrations and the range and accuracy for the application, tests were performed as written, and applicable test prerequisites were satisfied. Upon test completion, the inspectors considered whether the test results supported that equipment was capable of performing the required safety functions. The inspectors reviewed the following surveillance tests:

A isolation condenser test and calibration on April 1, 2015

B isolation condenser valve operability and in-service test (IST) on April 7, 2015 (IST)

Unidentified reactor coolant system (RCS) leak rate verification on May 7, 2015 (RCS)

B isolation condenser sensor test and calibration on May 8, 2015

Core spray system II valve operability and IST on May 19, 2015

b. Findings

No findings were identified.

Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation

.1 Training Observations

a. Inspection Scope

The inspectors observed a simulator training evolution for licensed operators on April 14, 2015, which required emergency plan implementation by an operations crew. Exelon planned for this evolution to be evaluated and included in performance indicator data regarding drill and exercise performance. The inspectors observed event classification and notification activities performed by the crew. The inspectors also attended the post-evolution critique for the scenario. The focus of the inspectors activities was to note any weaknesses and deficiencies in the crews performance and ensure that Exelon evaluators noted the same issues and entered them into the corrective action program.

b. Findings

No findings were identified.

RADIATION SAFETY

Cornerstone: Occupational and Public Radiation Safety

2RS5 Radiation Monitoring Instrumentation

a. Inspection Scope

The inspectors reviewed performance in assuring the accuracy and operability of radiation monitoring instruments used to protect occupational workers and for effluent monitoring and analysis. The inspectors used the requirements in 10 CFR 20; 10 CFR 50, Appendix I; technical specifications; Offsite Dose Calculation Manual (ODCM);regulatory guides; applicable industry standards; and procedures required by technical specifications as criteria for determining compliance.

Calibration and Testing Program

For the gaseous and liquid effluent radiation monitor instrumentation, the inspectors reviewed the current detector and electronic channel calibrations, functional testing results and alarm set-points.

b. Findings

No findings were identified.

2RS6 Radioactive Gaseous and Liquid Effluent Treatment

a. Inspection Scope

The inspectors reviewed the treatment, monitoring, and control of radioactive gaseous and liquid effluents. The inspectors used the requirements in 10 CFR 20; 10 CFR 50, Appendix I; technical specifications; ODCM; applicable industry standards; and procedures required by technical specifications as criteria for determining compliance.

Inspection Planning

The inspectors conducted in-office review of the Oyster Creek 2013 and 2014 annual radioactive effluent release reports, radioactive effluent program documents, UFSAR, ODCM, and applicable event reports.

Walk-downs and Observations

The inspectors walked down the gaseous and liquid radioactive effluent monitoring systems to assess the material condition and verify proper alignment according to plant design. The inspectors also observed potential unmonitored release points and reviewed radiation monitoring system surveillance records and the routine processing and discharge of gaseous and liquid radioactive wastes.

Sampling and Analyses

The inspectors reviewed: radioactive effluent sampling activities, representative sampling, compensatory sampling during effluent discharges with inoperable effluent radiation monitoring instrumentation, and the results of the inter-laboratory and intra-laboratory comparison program including scaling of hard-to-detect isotopes.

Effluent Flow Measuring Instruments

The inspectors reviewed the methodology used to determine the radioactive effluent stack and vent flow rates to verify that the flow rates were consistent with technical specification, ODCM, and UFSAR values.

Air Cleaning Systems

The inspectors reviewed radioactive effluent discharge system surveillance test results based on technical specification acceptance criteria.

Dose Calculations

The inspectors reviewed: changes in reported dose values from the previous annual radioactive effluent release reports, the scaling method for hard-to-detect radionuclides, ODCM changes, land use census changes, public dose calculations (monthly, quarterly, annual), and records of abnormal gaseous or liquid radioactive releases.

Groundwater Protection Initiative (GPI) Implementation

The inspectors reviewed: groundwater monitoring results, changes to the GPI program since the last inspection, anomalous results or missed groundwater samples, leakage or spill events including entries made into the decommissioning files (10 CFR 50.75(g)),

and Exelons evaluation of any positive groundwater sample results including appropriate stakeholder notifications and effluent reporting requirements.

Problem Identification and Resolution

The inspectors evaluated whether problems associated with the radioactive effluent monitoring and control program were identified at an appropriate threshold and properly addressed in the Exelons corrective action program.

b. Findings

No findings were identified.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification

.1 Unplanned Scrams, Unplanned Power Changes, and Unplanned Scrams with

Complications===

a. Inspection Scope

The inspectors reviewed Exelons submittals for the following Initiating Events cornerstone performance indicators for the period of April 1, 2014, through March 31, 2015.

Unplanned Scrams

Unplanned Power Changes

Unplanned Scrams with Complications

To determine the accuracy of the performance indicator data reported during those periods, inspectors used definitions and guidance contained in Nuclear Energy Institute (NEI) Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7. The inspectors reviewed Exelons operator narrative logs, maintenance planning schedules, condition reports, event reports, and NRC integrated inspection reports to validate the accuracy of the submittals.

b. Findings

No findings were identified.

.2 Safety System Functional Failures (1 sample)

c. Inspection Scope

The inspectors sampled Exelons submittals for the Safety System Functional Failures performance indicator for the period of April 1, 2014, through March 31, 2015. To determine the accuracy of the performance indicator data reported during those periods, inspectors used definitions and guidance contained in the NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, and NUREG-1022, Event Reporting Guidelines 10 CFR 50.72 and 10 CFR 50.73." The inspectors reviewed Exelons operator narrative logs, operability assessments, maintenance rule records, maintenance work orders, condition reports, event reports and NRC integrated inspection reports to validate the accuracy of the submittals.

d. Findings

No findings were identified.

4OA2 Problem Identification and Resolution

.1 Routine Review of Problem Identification and Resolution Activities

a. Inspection Scope

As required by Inspection Procedure 71152, Problem Identification and Resolution, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that Exelon entered issues into the corrective action program at an appropriate threshold, gave adequate attention to timely corrective actions, and identified and addressed adverse trends. In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the corrective action program and periodically attended condition report screening meetings. The inspectors also confirmed, on a sampling basis, that, as applicable, for identified defects and non-conformances, Exelon personnel performed an evaluation in accordance with 10 CFR Part 21.

b. Findings

No findings were identified.

.2 Semi-Annual Trend Review

a. Inspection Scope

The inspectors performed a semi-annual review of site issues to identify trends that might indicate the existence of more significant safety concerns. As part of this review, the inspectors included repetitive or closely-related issues that may have been documented by Exelon in trend reports, site performance indicators, major equipment problem lists, system health reports, and maintenance rule assessments, and maintenance or corrective action program backlogs. The inspectors also reviewed Exelons corrective action program database for the first and second quarters of 2015 to assess condition reports written in various subject areas (equipment problems, human performance issues, etc.), as well as individual issues identified during the NRCs daily condition report review.

b. Findings and Observations

No findings were identified.

The inspectors evaluated a sample of corrective maintenance backlogs, control room deficiency tags, open operability evaluations, and operator work-arounds. The inspectors verified that these issues were addressed within the scope of the corrective action program.

In addition, the inspectors reviewed a sampling of instrument out-of-tolerances within the last six months. The inspectors noted an apparent increase in the number of relay calibration drifts (i.e., did not meet as left condition). While a sample review by the inspectors indicated similar causal factors could not be identified, the increase in relay drifts should have warranted a more focused evaluation under station adverse rule procedures. In particular, other monitoring programs that complement the trending process, such as the instrument out-of-tolerance program, ER-AA-520, did not identify these relay malfunctions for further assessment. Exelon entered this issue into the corrective action program as issue report 2502999 for further review. The inspectors considered this a minor issue because there was not a trend of relay drifts beyond the as-found requirement specified in Technical Specifications.

4OA3 Follow-Up of Events and Notices of Enforcement Discretion

.1 Plant Events

a. Inspection Scope

For the plant events listed below, the inspectors reviewed and/or observed plant parameters, reviewed personnel performance, and evaluated performance of mitigating systems. The inspectors communicated the plant events to appropriate regional personnel, and compared the event details with criteria contained in IMC 0309, Reactive Inspection Decision Basis for Reactors, for consideration of potential reactive inspection activities. As applicable, the inspectors verified that Exelon made appropriate emergency classification assessments and properly reported the event in accordance with 10 CFR Parts 50.72 and 50.73. The inspectors reviewed Exelons follow-up actions related to the events to assure that Exelon implemented appropriate corrective actions commensurate with their safety significance.

RWCU system isolation due to operator error on March 26, 2015

Reactor scram caused by main transformer digital protection relay system actuation on May 7, 2015

b. Findings

Introduction:

A Green self-revealing NCV of Technical Specification 6.8.1(a),

Procedures and Programs, was identified because Exelon did not follow procedure 303, Reactor Cleanup Demineralizer System, during system restoration on March 26, 2015. Specifically, during startup from a forced outage (1F36), Exelon did not follow procedure 303, which required correct valve lineups for system restoration of RWCU after system isolation. This resulted in decreasing reactor water level, which was automatically terminated by a second RWCU isolation.

Description:

During shutdown and startup conditions, the RWCU system maintains water level in the reactor vessel to accommodate water inputs from the control rod drive system. During reactor startup and heatup activities on March 26, 2015, the RWCU system automatically isolated on high steam pressure of 136 psig (setpoint is 130 psig).

The operating crew was in the process of securing the auxiliary cleanup pump and placing the main cleanup recirculating pump in service as required by procedure 201, Plant Startup, and procedure 303, Reactor Cleanup Demineralizer System. The operators did not complete the procedure steps in time to prevent automatic system isolation as system pressure and reactor pressure increased due to the ongoing plant startup. The inspectors determined this automatic system isolation was not more than minor because vessel level increased as a result, which was in the conservative direction. Downstream of pressure control valve (PCV) ND-11, non-regenerative heat exchanger outlet pressure control valve, system piping is rated for 150 psig and system isolations are a protective feature to prevent piping failure and draining of the reactor water through the pipe failure. With the PCV ND-11 valve full open and the increase in reactor pressure due to startup activities, the system isolated as designed. As a result of the isolation, reactor level rose from 158 to 172 due to loss of letdown flow.

After the automatic RWCU isolation, operators implemented procedure 303, section 33, Restoring RWCU after an isolation with reactor pressure greater than 125 psig, to restore letdown flow. The procedure required verification of the correct system lineup, which included: confirming PCV ND-11 was in manual mode and closed and confirming that the system inlet valve, V-16-14, was in the closed position. However, the operators did not assure PCV ND-11 was closed prior to opening V-16-14 and, as a result, drained a portion of reactor water to the condensate suction header. Reactor level dropped from approximately 172 to 153 in a short period of time, and a second automatic isolation of RWCU occurred due to the system sensing high pressure. The automatic isolation terminated the level transient.

Exelon completed an apparent cause evaluation, under issue report 2474619, and determined that the Operations shift manager and unit supervisor shifted priority to immediately restore cleanup after the first automatic system isolation and the operators subsequently opened the V-16-14, which was not in accordance with procedure 303, section 33. The guidance in the procedure would have ensured that both V-16-14 and PCV ND-11 were in their correct lineup for the evolution and would have prevented the decrease in reactor vessel level. Exelons corrective actions included enhancing operator training in system knowledge and procedure compliance and revising startup procedures.

Analysis:

The failure to follow procedure 303 for restoration of RWCU after system isolation during plant startup is a performance deficiency that was reasonably within Exelons ability to foresee and correct. This finding is determined to be more than minor because it is associated with the human performance attribute of the Initiating Events cornerstone, and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, Exelon did not properly lineup the RWCU system after isolation, which resulted in a water level transient and challenging the critical safety function of inventory control.

The inspectors evaluated the finding using IMC 0609.04, Initial Characterization of Findings, and IMC 0609, Appendix A, Exhibit 1, Initiating Events Screening Questions.

The inspectors determined that this finding is a transient initiator that did not cause a reactor trip and loss of mitigation equipment relied upon to transition the plant from the onset of the trip to a stable shutdown condition. Therefore, the inspectors determined the finding to be of very low safety significance (Green).

This finding has a cross-cutting aspect in the area of Human Performance, Challenge the Unknown, because Exelon did not recognize and plan for the possibility of mistakes, or implement appropriate error reduction tools. Specifically, the operators did not stop and fully communicate plant condition after the initial RWCU isolation. Consequently, operators opened the RWCU system inlet valve due to the increasing water level without following procedure guidance. [H.11]

Enforcement:

Technical Specification 6.8.1(a), Procedures and Programs, states, in part, that written procedures shall be established, implemented and maintained covering the applicable procedures recommended in Appendix A of Regulatory Guide 1.33, Revision 2. Regulatory Guide 1.33, Appendix A, requires that safety related activities listed be covered in written procedures such as the reactor cleanup system. Contrary to the above, on March 26, 2015, Exelon did not properly implement the reactor cleanup system procedure. Specifically, Exelon did not follow procedure 303, section 33, Restoring RWCU after isolation with reactor pressure greater than 125 psig. As a result, reactor water level decreased approximately twenty inches in a short period of time. Exelons corrective actions included enhancing operator training in system knowledge and procedure compliance and revising startup procedures. Because this violation is of very low safety significance (Green) and was entered into Exelons corrective action program as issue report 2474619, this violation is being treated as an NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy. (NCV 05000219/2015002-03, Reactor Water Cleanup Procedure Not Followed Resulting in a Level Transient)

.2 (Closed) Licensee Event Report (LER) 05000219/2014-006-00:

Reactor SCRAM due to Decreasing Water Level

On October 12, 2014, during a plant startup from a refueling outage (1R25), and reactor power ascension at approximately 1 percent of rated thermal power, reactor water level began to lower. An automatic reactor scram occurred moments before operators inserted a manual scram in accordance with station procedures. Following the reactor scram, all systems operated as expected. At the time of the event, Exelon personnel were performing a post-maintenance test on the AVRs HMI. Exelon personnel reset the AVR controllers, which triggered logic to trip the turbine.

Exelon performed a root cause analysis on the event and determined station leadership inconsistently reinforced human performance error reduction, tool use, and procedure use and adherence. Exelon has taken steps to reduce these weaknesses in the future, which included the establishment of a performance improvement action plan focused on the human performance fundamentals.

The inspectors determined there was a self-revealing finding during the review of the LER (see below). This LER is closed.

a. Findings

.

Introduction.

A self-revealing Green finding was identified because Exelon did not properly screen work in accordance with MA-AA-716-010, Maintenance Planning.

Specifically, on September 12, 2014, Exelon did not screen the AVRs HMI post-maintenance test per the maintenance planning procedure. As a result, on October 12, 2014, Exelon personnel performing the post-maintenance test did not have a work order, which would have included plant configurations and limitations associated with the test.

This led to an automatic reactor scram.

Description.

On October 12, 2014, while the plant was at approximately 1 percent power during plant startup following refueling outage (1R25), a reactor scram occurred due to low level in the reactor vessel.

A portion of the outage scope was to troubleshoot and repair the AVRs HMI computer following issues with the software. The purpose of the AVR is to regulate main generator output voltage. A contractor was tasked to perform a post-maintenance test following the troubleshooting to ensure the HMI was properly communicating with the AVR controllers per Exelon procedure 421, EX2100e HMI, Trouble and Fault Alarms.

During the post-maintenance test, the contractor recognized that the HMI was communicating with the M2 controller but not the M1 controller. At this point, the contractor should have stopped work and noted the deviation from the expected result as a failed post-maintenance test. However, the contractor directed the electrical technician to continue work and reset the M1 controller. This action did not restore communication between the AVR and HMI. The contractor then directed the electrical technician to reset all three AVR controllers: M1, M2, and C. The reset of the three AVR controllers triggered the logic to trip the turbine. The reactor protection system received a reactor low level signal, which caused an automatic reactor scram. The plant responded as expected.

On September 12, 2014, when Exelon added this activity into the scope of the outage, Exelon personnel did not properly screen the work activity to determine if the post-maintenance test required a work order per MA-AA-716-010, Maintenance Planning.

Instead, the activity was performed under an action request, which did not include requirements for precautions and limitations, and a pre-job brief was not performed. Per MA-AA-716-010, the work was required to be a Level 1 activity due to the location and work to be performed. Specifically, table 2 in MA-AA-716-010 Work Package Usage Based on Type of Work Activity and Location, states, in part, a post-maintenance testing work activity performed in the power block requires a Level 1 or Level 2 work package. MA-AA-716-010, Attachment 6, Graded Approach to Planning Decision Tree for Work Package Level Determination, states in part, post-maintenance testing in the power block that is complex or infrequently performed requires a Level 1 work package.

MA-AA-716-010 defines infrequent as greater than 12 months. Had the post-maintenance test been properly categorized as an infrequent activity, according to MA-AA-716-010, a Level 1 activity would require a detailed work package. Per MA-AA-716-010, Attachment 6, a detailed work package states minimum expected content to include, in part, precautions and limitations and a pre-job brief. Exelon completed a root cause evaluation, which stated, in part, Per MA-AA-716-010, Maintenance Planning, and MA-AA-716-235, Control of Critical Digital Asset Portable Media and Portable Devices, a work order was required for this activity.

Per HU-AA-1211, Pre-job Briefings, standard pre-job briefings are conducted for low risk, infrequent activities and include contingencies and stop-work criteria. If a pre-job brief had been performed, it should have discussed Exelon personnel actions if the HMI failed to respond as expected. A proper work package should have provided barriers to prevent Exelon from working beyond the scope of the post-maintenance test such as following a stop-work criteria.

HU-AA-101, Human Performance Tools and Verification Practices, Step 4.1.3 states, in part, personnel should stop if they find themselves outside of procedures, parameters, or processes when unexpected post-maintenance test results are received. Attachment 4 of HU-AA-101 defines one example of stop-work criteria as a work performance issues, specifically equipment that does not respond as expected. Had HU-AA-101 been implemented, Exelon personnel should have stopped the post-maintenance test when the HMI screen did not respond as expected, thus preventing the automatic reactor scram.

Analysis.

The failure to properly screen the HMI work per MA-AA-716-010 is a performance deficiency that was within Exelons ability to foresee and correct. This finding is determined to be more than minor because it is associated with the human performance attribute of the Initiating Events cornerstone and affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during power operation. Specifically, resetting the three AVR controllers caused an automatic reactor scram. The inspectors evaluated the finding using IMC 0609.04, Initial Characterization of Findings, and IMC 0609, Appendix A, Exhibit 1, Initiating Events Screening Questions. The inspectors determined that this finding was a transient initiator that did not cause a reactor trip and loss of mitigation equipment relied upon to transition the plant from the onset of the trip to a stable shutdown condition. Therefore, the inspectors determined the finding to be of very low safety significance (Green).

This finding has a cross cutting aspect in the area of Human Performance associated with Challenge the Unknown, because Exelon personnel did not stop when faced with uncertain situations. Specifically, on October 12, 2014, Exelon personnel did not stop when faced with the uncertain situation of the HMI screen not responding as expected.

[H.11]

Enforcement.

This finding does not involve enforcement action because no violation of regulatory requirements violation was identified. Exelon entered this issue into their corrective action program as issue report 2394374. Because this issue does not involve a violation and has very low safety significance, it is identified as a finding. (FIN 05000219/2015002-04, Reset of the Automatic Voltage Regulator Controllers Led to an Automatic Reactor Scram)

4OA6 Meetings, Including Exit

On July 10, 2015, the inspectors presented the inspection results to Mr. G. Stathes, Site Vice President, and other members of the Oyster Creek staff. The inspectors verified that no proprietary information was retained by the inspectors or documented in this report.

ATTACHMENT:

SUPPLEMENTARY INFORMATION

KEY POINTS OF CONTACT

Exelon Personnel

G. Stathes, Site Vice President
J. Dostal, Plant Manager
M. Ford, Director, Operations
J. Stanley, Director, Engineering
D. Chernesky, Director, Maintenance
C. Symonds, Director, Training
D. DiCello, Director, Work Management
M. McKenna, Manager, Regulatory Assurance
T. Farenga, Radiation Protection Manager
J. Renda, Manager, Environmental/Chemistry
T. Keenan, Manager, Site Security
P. Bloss, Senior Manager, Plant Engineering
H. Ray, Senior Manager, Design Engineering
E. Swain, Shift Operations Superintendent
T. Cappuccino, Senior Regulatory Assurance Specialist
K. Wolfe, Manager, Health Physics
J. McCarthy, Senior Radiological Engineer
M. Nixon, Chemist - RETS/REMP
J. Eagan, Manager, Operations Training
G. Young, LORT Exam Author
J. Gessner, LORT Exam Author
M. Rossi, LORT Lead

LIST OF ITEMS OPENED, CLOSED, DISCUSSED, AND UPDATED

Opened/Closed

05000219/2015002-01 FIN Inadequate Assessment of 4k Emergency Switchgear Roll-Up Door Degraded Floor Gasket (Section 1R06)
05000219/2015002-02 FIN Failure Rates Exceed Twenty Percent for Annual Requalification Exam (Section 1R11)
05000219/2015002-03 NCV Reactor Water Cleanup Procedure Not Followed Resulting in a Level Transient (Section 4OA3)
05000219/2015002-04 FIN Reset of the Automatic Voltage Regulator Controller Led to an Automatic Reactor Scram (Section 4OA3)

Closed

05000219/2014-006-00 LER Reactor SCRAM Due to Decreasing Water Level (Section 4OA3)

LIST OF DOCUMENTS REVIEWED