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| number = ML16258A175
| number = ML16258A175
| issue date = 09/14/2016
| issue date = 09/14/2016
| title = Millstone Power Station - NRC Triennial Fire Protection Inspection Report 05000336/2016007 and 05000423/2016007
| title = NRC Triennial Fire Protection Inspection Report 05000336/2016007 and 05000423/2016007
| author name = Cahill C G
| author name = Cahill C
| author affiliation = NRC/RGN-I/DRS/EB3
| author affiliation = NRC/RGN-I/DRS/EB3
| addressee name = Heacock D A
| addressee name = Heacock D
| addressee affiliation = Dominion Resources, Inc
| addressee affiliation = Dominion Resources, Inc
| docket = 05000336, 05000423
| docket = 05000336, 05000423
Line 14: Line 14:
| page count = 37
| page count = 37
}}
}}
See also: [[followed by::IR 05000336/2016007]]
See also: [[see also::IR 05000336/2016007]]


=Text=
=Text=
{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION REGION I 2100 RENAISSANCE BLVD. KING OF PRUSSIA, PA  19406-2713  
{{#Wiki_filter:UNITED STATES  
NUCLEAR REGULATORY COMMISSION  
REGION I  
2100 RENAISSANCE BLVD.  
KING OF PRUSSIA, PA  19406-2713  
   
   
  September 14, 2016  
  Mr. David A. Heacock  
September 14, 2016  
   
Mr. David A. Heacock  
President and Chief Nuclear Officer  
President and Chief Nuclear Officer  
Dominion Resources 5000 Dominion Boulevard  
Dominion Resources  
 
5000 Dominion Boulevard  
Glen Allen, VA  23060-6711  
Glen Allen, VA  23060-6711  
   
   
SUBJECT: MILLSTONE POWER STATION - NRC TRIENNIAL FIRE PROTECTION INSPECTION REPORT 05000336/2016007 AND 05000423/2016007  
SUBJECT:  
  Dear Mr. Heacock:  
MILLSTONE POWER STATION - NRC TRIENNIAL FIRE PROTECTION  
 
INSPECTION REPORT 05000336/2016007 AND 05000423/2016007  
   
Dear Mr. Heacock:  
   
   
On August 11, 2016, the U.S. Nuclear Regulatory Commission (NRC) completed a triennial fire  
On August 11, 2016, the U.S. Nuclear Regulatory Commission (NRC) completed a triennial fire  
protection inspection at Millstone Power Station, Units 2 and 3.  The enclosed inspection report documents the inspection results, which were discussed on August 11, 2016, with Mr. John Daugherty, Site Vice President - Millstone Power Station, and other members of your staff.  
protection inspection at Millstone Power Station, Units 2 and 3.  The enclosed inspection report  
 
documents the inspection results, which were discussed on August 11, 2016, with Mr. John  
Daugherty, Site Vice President - Millstone Power Station, and other members of your staff.  
   
   
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations, and with the conditions of your license.  The inspectors reviewed selected procedures and records, observed activities, and interviewed station personnel.  The inspectors also reviewed mitigation strategies for addressing large fires and explosions.  
The inspection examined activities conducted under your license as they relate to safety and  
 
compliance with the Commission's rules and regulations, and with the conditions of your  
license.  The inspectors reviewed selected procedures and records, observed activities, and  
interviewed station personnel.  The inspectors also reviewed mitigation strategies for addressing  
large fires and explosions.  
   
   
Based on the results of this inspection, one finding of very low safety significance (Green) was  
Based on the results of this inspection, one finding of very low safety significance (Green) was  
identified.  This finding was determined to be a violation of NRC requirements.  However, because of its very low safety significance, and because it was entered into your corrective action program, the NRC is treating this finding as a non-cited violation (NCV) consistent with  
identified.  This finding was determined to be a violation of NRC requirements.  However,  
because of its very low safety significance, and because it was entered into your corrective  
action program, the NRC is treating this finding as a non-cited violation (NCV) consistent with  
Section 2.3.2 of the NRC Enforcement Policy.  If you contest any NCV in this report, you should  
Section 2.3.2 of the NRC Enforcement Policy.  If you contest any NCV in this report, you should  
provide a written response within 30 days of the date of this inspection report, with the basis for  
provide a written response within 30 days of the date of this inspection report, with the basis for  
your denial, to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington D.C. 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement; and the NRC Resident Inspector at Millstone Power Stations.  
your denial, to the Nuclear Regulatory Commission, ATTN: Document Control Desk,  
Washington D.C. 20555-0001; with copies to the Regional Administrator, Region I; the Director,  
Office of Enforcement; and the NRC Resident Inspector at Millstone Power Stations.  


D. Heacock
2
In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390 of the NRC's
"Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be
available electronically for public inspection in the NRC Public Document Room or from the
Publicly Available Records System (PARS) component of the NRC's document system,
Agencywide Documents Access and Management System (ADAMS).  ADAMS is accessible
from the NRC Web Site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic
Reading Room).
Sincerely,
   
   
 
/RA/  
D. Heacock 2
In accordance with Title 10 of the Code of Federal Regulations
(10 CFR) 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be
available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records System (PARS) component of the NRC's document system, Agencywide Documents Access and Management System (ADAMS).  ADAMS is accessible
from the NRC Web Site at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
   
   
Sincerely,              /RA/
Christopher G. Cahill  
Christopher G. Cahill  
 
Acting Branch Chief  
Acting Branch Chief  
Engineering Branch 3  
Engineering Branch 3  
Division of Reactor Safety  
Division of Reactor Safety  
   
   
Docket Nos. 50-336, 50-423  
Docket Nos.  
50-336, 50-423  
License Nos. DPR-65, NPF-49  
License Nos. DPR-65, NPF-49  
 
Enclosure: Inspection Report 05000336/2016007  
Enclosure:  
Inspection Report 05000336/2016007  
   and 05000423/2016007   
   and 05000423/2016007   
w/Attachment:  Supplemental Information  
w/Attachment:  Supplemental Information  
cc w/encl:  Distribution via ListServ


cc w/encl:  Distribution via ListServ
 


  ML16258A175  SUNSI Review  
  ML16258A175  
  Non-Sensitive  
  SUNSI Review  
    Publicly Available  
  OFFICE RI/DRS RI/DRS RI/DRP RI/DRS  NAME JPatel WCook GDentel CCahill  DATE 09/09/16 09/09/16 09/09/16 09/14/16
Non-Sensitive  
Publicly Available  
OFFICE  
RI/DRS  
RI/DRS  
RI/DRP  
RI/DRS  
   
NAME  
JPatel  
WCook  
GDentel  
CCahill  
   
DATE  
09/09/16  
09/09/16  
09/09/16  
09/14/16  
   
   
  i Enclosure
U.S. NUCLEAR REGULATORY COMMISSION
REGION I 
Docket Nos.:  50-336, 50-423


   
   
   
   
License Nos.:  DPR-65, NPF-49  
i
 
Enclosure
Report Nos.:  05000336/2016007 and 05000423/2016007  
 
U.S. NUCLEAR REGULATORY COMMISSION
REGION I
Docket Nos.: 
50-336, 50-423
License Nos.:   
DPR-65, NPF-49  
Report Nos.:   
05000336/2016007 and 05000423/2016007  
Licensee:
Dominion Nuclear Connecticut, Inc.
Facility:
Millstone Power Station, Units 2 and 3
Location:
P.O. Box 128
Waterford, CT  06385
Dates: 
July 25, 2016 through August 11, 2016
Inspectors:
J. Patel, Reactor Inspector (Team Leader) 
Division of Reactor Safety (DRS)
W. Cook, Senior Reactor Analyst, DRS
E. DiPaolo, Senior Reactor Inspector, DRS
D. Orr, Senior Reactor Inspector, DRS
K. Young, Senior Reactor Inspector, DRS
L. Dumont, Reactor Inspector, DRS
S. Galbreath, Reactor Inspector, DRS
J. Rady, Reactor Inspector, DRS
Observers:
S. Freeman, Senior Reactor Analyst, NRC, Region II, DRS
   
   
Licensee:  Dominion Nuclear Connecticut, Inc.
   
   
Approved by: 
Chris Cahill, Acting Branch Chief
Engineering Branch 3
Division of Reactor Safety
   
   
Facility:  Millstone Power Station, Units 2 and 3


   
   
  Location:  P.O. Box 128    Waterford, CT  06385
   
 
ii
   
   
   
   
Dates:  July 25, 2016 through August 11, 2016
SUMMARY OF FINDINGS
 
Inspectors:  J. Patel, Reactor Inspector (Team Leader) 
  Division of Reactor Safety (DRS)
  W. Cook, Senior Reactor Analyst, DRS
  E. DiPaolo, Senior Reactor Inspector, DRS    D. Orr, Senior Reactor Inspector, DRS    K. Young, Senior Reactor Inspector, DRS
  L. Dumont, Reactor Inspector, DRS
  S. Galbreath, Reactor Inspector, DRS J. Rady, Reactor Inspector, DRS
Observers:  S. Freeman, Senior Reactor Analyst, NRC, Region II, DRS
   
   
Approved by:  Chris Cahill, Acting Branch Chief Engineering Branch 3
IR 05000336/2016007, 05000423/2016007; 07/25/2016 - 08/11/2016; Dominion Nuclear  
Division of Reactor Safety
 
  ii  SUMMARY OF FINDINGS
IR 05000336/2016007, 05000423/2016007; 07/25/2016 - 08/11/2016; Dominion Nuclear  
Connecticut, Inc.; Millstone Power Station, Units 2 and 3; Fire Protection (Triennial).  
Connecticut, Inc.; Millstone Power Station, Units 2 and 3; Fire Protection (Triennial).  
   
   
This report covered a two week on-site triennial fire protection team inspection by specialist inspectors.  One finding of very low safety significance was identified.  This finding was determined to be a non-cited violation.  The significance of most findings is indicated by their  
This report covered a two week on-site triennial fire protection team inspection by specialist  
color (Green, While, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process." The cross-cutting aspects associated with findings were determined  
inspectors.  One finding of very low safety significance was identified.  This finding was  
determined to be a non-cited violation.  The significance of most findings is indicated by their  
color (Green, While, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance  
Determination Process.  The cross-cutting aspects associated with findings were determined  
using IMC 0310, "Components Within The Cross-Cutting Areas."  Findings for which the  
using IMC 0310, "Components Within The Cross-Cutting Areas."  Findings for which the  
significance determination process (SDP) does not apply may be Green or be assigned a severity level after NRC management review.  The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 6, dated July 2016.  
significance determination process (SDP) does not apply may be Green or be assigned a  
 
severity level after NRC management review.  The NRC's program for overseeing the safe  
Cornerstone:  Mitigating Systems
operation of commercial nuclear power reactors is described in NUREG-1649, Reactor  
  Green.  The team identified a finding of very low safety significance (Green) involving a non-cited violation of Millstone Power Station, Unit 2, Renewed Facility Operating License Condition 2.C.(3) to implement and maintain in effect all provisions of the approved fire  
Oversight Process, Revision 6, dated July 2016.  
protection program as described in the Final Safety Analysis Report (FSAR).  Specifically, Dominion failed to maintain the #2 steam generator (SG) atmospheric dump valve (ADV)  
Cornerstone:  Mitigating Systems  
Green.  The team identified a finding of very low safety significance (Green) involving a non-
cited violation of Millstone Power Station, Unit 2, Renewed Facility Operating License  
Condition 2.C.(3) to implement and maintain in effect all provisions of the approved fire  
protection program as described in the Final Safety Analysis Report (FSAR).  Specifically,  
Dominion failed to maintain the #2 steam generator (SG) atmospheric dump valve (ADV)  
free from fire damage, which may have affected the availability to maintain hot shutdown  
free from fire damage, which may have affected the availability to maintain hot shutdown  
conditions from the main control room for a fire in Fire Area R-14, Lower 4.16kV Switchgear Room and Cable Vault.
conditions from the main control room for a fire in Fire Area R-14, Lower 4.16kV Switchgear  
  Dominion promptly entered this safe shutdown issue into their corrective action program as condition report (CR) 1043458.  Immediate corrective actions included implementing compensatory measures in the form of fire watches for fire area R-14  
Room and Cable Vault. Dominion promptly entered this safe shutdown issue into their  
corrective action program as condition report (CR) 1043458.  Immediate corrective actions  
included implementing compensatory measures in the form of fire watches for fire area R-14  
that are being tracked by Reasonable Assurance of Safety (RAS) determination 3037040.   
that are being tracked by Reasonable Assurance of Safety (RAS) determination 3037040.   
 
Longer term corrective actions included submitting an exemption request to the NRC for use  
Longer term corrective actions included submitting an exemption request to the NRC for use of a local operator manual action (OMA) to operate the #2 SG ADV in lieu of meeting fire protection requirements for fire area R-14.  The team considered Dominion's immediate and  
of a local operator manual action (OMA) to operate the #2 SG ADV in lieu of meeting fire  
protection requirements for fire area R-14.  The team considered Dominions immediate and  
longer term corrective actions appropriate.  
longer term corrective actions appropriate.  
  The performance deficiency was more than minor because it affected the Mitigating  
   
Systems cornerstone objective to ensure the availability, reliability, and capability of systems that respond to an external event to prevent undesirable consequences in the event of a fire.  Specifically, the use of an OMA during post-fire safe shutdown is not as reliable as normal  
The performance deficiency was more than minor because it affected the Mitigating  
Systems cornerstone objective to ensure the availability, reliability, and capability of systems  
that respond to an external event to prevent undesirable consequences in the event of a fire.   
Specifically, the use of an OMA during post-fire safe shutdown is not as reliable as normal  
systems operation which could be utilized had the requirements of 10 CFR Part 50,  
systems operation which could be utilized had the requirements of 10 CFR Part 50,  
Appendix R, Section III.G.2 been met and, therefore, prevented fire damage to credited  
Appendix R, Section III.G.2 been met and, therefore, prevented fire damage to credited  
components and/or cables, specifically the #2 SG ADV.  The inspectors used IMC 0609, Appendix F, Fire Protection Significance Determination Process, Phase 1 and determined the reactor is able to reach and maintain a hot safe shutdown condition because the SG  
components and/or cables, specifically the #2 SG ADV.  The inspectors used IMC 0609,  
ADVs are used for transition to cold shutdown, therefore this finding was of very low safety significance (Green).  This finding does not have a cross cutting aspect because the  
Appendix F, Fire Protection Significance Determination Process, Phase 1 and determined  
the reactor is able to reach and maintain a hot safe shutdown condition because the SG  
ADVs are used for transition to cold shutdown, therefore this finding was of very low safety  
significance (Green).  This finding does not have a cross cutting aspect because the  
performance deficiency occurred greater than three years ago when the June 30, 2011  
performance deficiency occurred greater than three years ago when the June 30, 2011  
exemption request letter to the NRC was supplemented by letter on February 29, 2012, and is not indicative of current licensee performance.  (Section 1R05.01)   
exemption request letter to the NRC was supplemented by letter on February 29, 2012, and  
  iii   Other Findings  
is not indicative of current licensee performance.  (Section 1R05.01)  
  Three violations of very low safety significance that were identified by Dominion were reviewed by the team.  Corrective actions taken or planned by Dominion have been entered into  
 
Dominion's corrective action program (CAP).  The violations and corrective action tracking  
   
iii  
Other Findings  
   
Three violations of very low safety significance that were identified by Dominion were reviewed  
by the team.  Corrective actions taken or planned by Dominion have been entered into  
Dominions corrective action program (CAP).  The violations and corrective action tracking  
numbers are listed in Section 4OA7 of this report.  
numbers are listed in Section 4OA7 of this report.  
 
 
  REPORT DETAILS  
  Background  
 
REPORT DETAILS  
   
Background  
   
   
This report presents the results of a triennial fire protection inspection conducted in accordance  
This report presents the results of a triennial fire protection inspection conducted in accordance  
with the U.S. Nuclear Regulatory Commission (NRC) Inspection Procedure (IP) 71111.05T,  
with the U.S. Nuclear Regulatory Commission (NRC) Inspection Procedure (IP) 71111.05T,  
"Fire Protection (Triennial)." The objective of the inspection was to assess whether Dominion  
Fire Protection (Triennial).  The objective of the inspection was to assess whether Dominion  
Nuclear Connecticut, Inc. (Dominion) has implemented an adequate fire protection program  
Nuclear Connecticut, Inc. (Dominion) has implemented an adequate fire protection program  
(FPP) and that post-fire safe shutdown capabilities have been established and are being properly maintained at the Millstone Power Station Unit 2 and Unit 3 (Millstone).  The following fire areas (FA) and/or fire zones (FZ) were selected for detailed review based on risk insights  
(FPP) and that post-fire safe shutdown capabilities have been established and are being  
from the Millstone Individual Plant Exam
properly maintained at the Millstone Power Station Unit 2 and Unit 3 (Millstone).  The following  
ination of External Events (IPEEE).  
fire areas (FA) and/or fire zones (FZ) were selected for detailed review based on risk insights  
  Unit 2 Fire Areas / Fire Zones  
from the Millstone Individual Plant Examination of External Events (IPEEE).  
  R-7 / A-15, "A" Diesel Generator Room A  R-1 / A-32, Main Ventilation Room (Air Handling Units)  R-14 / T-7, 6.9 & 4.16 kV Switchgear Room  R-14 / T-9, East Cable Vault  
  Unit 3 Fire Areas  
  AB-6, West MCC & Rod Control Area  CB-11, Instrument Rack Room and Underfloor Area  EG-3, North Emergency Generator Enclosure  ESF-3, North Residual Heat Removal - Heat Exchanger Cubicle  
Unit 2 Fire Areas / Fire Zones  
  Inspection of these areas/zones fulfills the inspection procedure requirement to inspect a  
R-7 / A-15, A Diesel Generator Room A  
   
R-1 / A-32, Main Ventilation Room (Air Handling Units)  
   
R-14 / T-7, 6.9 & 4.16 kV Switchgear Room  
   
R-14 / T-9, East Cable Vault  
   
Unit 3 Fire Areas  
AB-6, West MCC & Rod Control Area  
   
CB-11, Instrument Rack Room and Underfloor Area  
   
EG-3, North Emergency Generator Enclosure  
   
ESF-3, North Residual Heat Removal - Heat Exchanger Cubicle  
   
Inspection of these areas/zones fulfills the inspection procedure requirement to inspect a  
minimum of three samples.  
minimum of three samples.  
  The inspection team evaluated Dominion's FPP against applicable requirements which included  
   
The inspection team evaluated Dominions FPP against applicable requirements which included  
Unit 2 Renewed Facility Operating License Condition 2.C.(3), Unit 3 Renewed Facility Operating  
Unit 2 Renewed Facility Operating License Condition 2.C.(3), Unit 3 Renewed Facility Operating  
License Conditions 2.H, NRC Safety Evaluation Reports (SERs), Title 10 of the  
License Conditions 2.H, NRC Safety Evaluation Reports (SERs), Title 10 of the Code of Federal  
Code of Federal  
Regulations (10 CFR) 50.48, 10 CFR Part 50, Appendix R and Branch Technical Position (BTP)  
Regulations (10 CFR) 50.48, 10 CFR Part 50, Appendix R and Branch Technical Position (BTP) Chemical Engineering Branch (CMEB) 9.5-1.   
Chemical Engineering Branch (CMEB) 9.5-1.  The team also reviewed related documents that  
The team also reviewed related documents that included the Updated Final Safety Analysis Repor
included the Updated Final Safety Analysis Report (UFSAR), Fire Protection Program, Fire  
t (UFSAR), Fire Protection Program, Fire  
Hazards Analyses (FHA), and post-fire Safe Shutdown Analyses Reports.  
Hazards Analyses (FHA), and post-fire Safe Shutdown Analyses Reports.  
   
   
The team also evaluated two Unit 2 and two Unit 3 licensee mitigating strategies for addressing  
The team also evaluated two Unit 2 and two Unit 3 licensee mitigating strategies for addressing  
large fires and explosions as required by Unit 2 Renewed Facility Operating License Condition 2.C.(13), Unit 3 Renewed Facility Operating License Condition 2.C.(10), and 10 CFR 50.54 (hh)(2).  Inspection of these strategies fulfills the inspection procedure requirement to inspect a minimum of one sample.  
large fires and explosions as required by Unit 2 Renewed Facility Operating License Condition  
2.C.(13), Unit 3 Renewed Facility Operating License Condition 2.C.(10), and 10 CFR 50.54  
(hh)(2).  Inspection of these strategies fulfills the inspection procedure requirement to inspect a  
minimum of one sample.  
Specific documents reviewed by the team are listed in the Attachment to this report.


2
1.
REACTOR SAFETY
Cornerstones:  Initiating Events, Mitigating Systems, and Barrier Integrity
1R05 Fire Protection (IP 71111.05T) 
.01
Protection of Safe Shutdown Capabilities
  a.
Inspection Scope 
   
   
Specific documents reviewed by the team are listed in the Attachment to this report.
The team reviewed the FHA, safe shutdown analyses, and supporting drawings and  
 
documentation to verify that post-fire safe shutdown capabilities were properly protected.   
2  1. REACTOR SAFETY
The team ensured that applicable separation requirements of Section III.G of 10 CFR  
Cornerstones:  Initiating Events, Mitigating Systems, and Barrier Integrity
Part 50, Appendix R for Unit 2 and BTP CMEB 9.5-1 for Unit 3 as well as the licensees
1R05 Fire Protection (IP 71111.05T) 
.01 Protection of Safe Shutdown Capabilities
  a. Inspection Scope 
The team reviewed the FHA, safe shutdown analyses, and supporting drawings and documentation to verify that post-fire safe shutdown capabilities were properly protected.  The team ensured that applicable separation requirements of Section III.G of 10 CFR  
Part 50, Appendix R for Unit 2 and BTP CMEB 9.5-1 for Unit 3 as well as the licensee's
design and licensing bases were maintained for the credited safe shutdown equipment  
design and licensing bases were maintained for the credited safe shutdown equipment  
and their supporting power, control, and instrumentation cables.  This review included an  
and their supporting power, control, and instrumentation cables.  This review included an  
assessment of the adequacy of the selected systems for reactivity control, reactor coolant makeup, reactor heat removal, process monitoring, and associated support system functions.  
assessment of the adequacy of the selected systems for reactivity control, reactor  
coolant makeup, reactor heat removal, process monitoring, and associated support  
system functions.  
    b.
Findings
   
   
    b. Findings
Introduction:  The team identified a finding of very low safety significance (Green)  
Introduction:  The team identified a finding of very low safety significance (Green) involving a non-cited violation of Millstone Unit 2 Renewed Facility Operating License Condition 2.C.(3) to implement and maintain in effect all provisions of the approved fire  
involving a non-cited violation of Millstone Unit 2 Renewed Facility Operating License  
Condition 2.C.(3) to implement and maintain in effect all provisions of the approved fire  
protection program as described in the FSAR.  Specifically, Dominion failed to maintain  
protection program as described in the FSAR.  Specifically, Dominion failed to maintain  
the #2 SG ADV free from fire damage, which may have affected the availability to maintain hot shutdown conditions from the main control room for a fire in Fire Area R-14, Lower 4.16kV Switchgear Room and Cable Vault.  
the #2 SG ADV free from fire damage, which may have affected the availability to  
  Description:  The inspectors reviewed the operator manual actions (OMAs) contained in operating procedure AOP 2579M, Fire Procedure for Hot Standby Appendix R Fire Area  
maintain hot shutdown conditions from the main control room for a fire in Fire Area R-14,  
R-14, and compared them against the list of NRC approved OMAs in lieu of meeting III.G.2 fire protection requirements and determined that an unapproved OMA was being implemented in AOP 2579M.  The OMAs in  
Lower 4.16kV Switchgear Room and Cable Vault.  
lieu of meeting III.G.2 fire protection requirements were approved in an NRC exemption dated December 18, 2012.  The  
   
Description:  The inspectors reviewed the operator manual actions (OMAs) contained in  
operating procedure AOP 2579M, Fire Procedure for Hot Standby Appendix R Fire Area  
R-14, and compared them against the list of NRC approved OMAs in lieu of meeting  
III.G.2 fire protection requirements and determined that an unapproved OMA was being  
implemented in AOP 2579M.  The OMAs in lieu of meeting III.G.2 fire protection  
requirements were approved in an NRC exemption dated December 18, 2012.  The  
missing OMA was an action to locally operate air-operated valve, 2-MS-190B, #2 SG  
missing OMA was an action to locally operate air-operated valve, 2-MS-190B, #2 SG  
ADV.  The OMA is necessary since a self-induced loss of offsite power (LOOP) will occur and station blackout (SBO) condition may occur from fire related cable damage.  Either condition, LOOP or SBO, will cause a loss of instrument air in response to a  
ADV.  The OMA is necessary since a self-induced loss of offsite power (LOOP) will  
occur and station blackout (SBO) condition may occur from fire related cable damage.   
Either condition, LOOP or SBO, will cause a loss of instrument air in response to a  
significant fire in fire area R-14.  
significant fire in fire area R-14.  
  The LOOP will occur when AOP 2579M is implemented because step 3.4 requires the  
   
operators to trip the reactor (causing a loss of the normal station service transformer) and step 3.9 requires the operators to direct CONVEX (transmission operator) to de-energize the reserve station service transformer.  A SBO may subsequently occur if the  
The LOOP will occur when AOP 2579M is implemented because step 3.4 requires the  
operators to trip the reactor (causing a loss of the normal station service transformer)  
and step 3.9 requires the operators to direct CONVEX (transmission operator) to de-
energize the reserve station service transformer.  A SBO may subsequently occur if the  
B emergency diesel generator (EDG) is running and its output breaker does not close,   
B emergency diesel generator (EDG) is running and its output breaker does not close,   
 
3  which could occur due to fire-related circuit damage. In either condition, LOOP or SBO, the 'F' instrument air compressor, will be de-energized and a loss of instrument air will
   


occur.  In 2011, Dominion submitted an exemption request to the NRC for several OMAs in lieu of meeting III.G.2 fire protection requirements in several fire areas and initially postulated a loss of instrument air for Fire Area R-14.  Three OMAs were requested related to the  
3
which could occur due to fire-related circuit damage.  In either condition, LOOP or SBO,
the F instrument air compressor, will be de-energized and a loss of instrument air will
occur.  
   
In 2011, Dominion submitted an exemption request to the NRC for several OMAs in lieu  
of meeting III.G.2 fire protection requirements in several fire areas and initially postulated  
a loss of instrument air for Fire Area R-14.  Three OMAs were requested related to the  
loss of instrument air for Fire Area R-14 in a June 30, 2011 exemption request letter to  
loss of instrument air for Fire Area R-14 in a June 30, 2011 exemption request letter to  
the NRC.  Subsequent to the June 30, 2011 exemption request letter, Dominion walked  
the NRC.  Subsequent to the June 30, 2011 exemption request letter, Dominion walked  
down several fire areas and from a mechanical perspective concluded that a loss of instrument air should no longer be postulated for several fire areas.  R-14 was included as a fire area for which a loss of instrument air was no longer considered credible.  In a  
down several fire areas and from a mechanical perspective concluded that a loss of  
instrument air should no longer be postulated for several fire areas.  R-14 was included  
as a fire area for which a loss of instrument air was no longer considered credible.  In a  
request for additional information response letter dated February 29, 2012, Dominion  
request for additional information response letter dated February 29, 2012, Dominion  
stated that the loss of instrument air was no longer postulated in fire area R-14 and  
stated that the loss of instrument air was no longer postulated in fire area R-14 and  
others, and requested the NRC delete the OMA for  
others, and requested the NRC delete the OMA for locally operating the #2 SG ADV.  In  
locally operating the #2 SG ADV.  In a correction letter dated October 29, 2012, Dominion again reiterated that for Fire Area R-14, and others, a Loss of Instrument Air was not postulated, but Dominion clarified that some of the OMAs that were related to a loss of instrument air should be retained  
a correction letter dated October 29, 2012, Dominion again reiterated that for Fire Area  
R-14, and others, a Loss of Instrument Air was not postulated, but Dominion clarified  
that some of the OMAs that were related to a loss of instrument air should be retained  
for postulated fire cable damage or loss of power.  However, the OMA for locally  
for postulated fire cable damage or loss of power.  However, the OMA for locally  
operating the #2 SG ADV was not retained since it was not susceptible to cable damage  
operating the #2 SG ADV was not retained since it was not susceptible to cable damage  
or loss of power for a fire in area R-14.  Dominion stated in its June 30, 2011 exemption request letter to the NRC that after auxiliary feedwater (AFW) is established from the control room, operation of the ADV (2-MS-1 90B) is the required method of removing  
or loss of power for a fire in area R-14.  Dominion stated in its June 30, 2011 exemption  
request letter to the NRC that after auxiliary feedwater (AFW) is established from the  
control room, operation of the ADV (2-MS-1 90B) is the required method of removing  
decay heat to maintain hot standby and transition to cold shutdown.  
decay heat to maintain hot standby and transition to cold shutdown.  
  As described above, the inspectors determined that implementing AOP 2579M as  
   
written will cause a loss of instrument air and the OMA to locally operate the #2 SG ADV will be necessary after AFW is restored and decay heat removal is transitioned from the main steam safety valves to the #2 SG ADV for steam generator pressure control.  The  
As described above, the inspectors determined that implementing AOP 2579M as  
written will cause a loss of instrument air and the OMA to locally operate the #2 SG ADV  
will be necessary after AFW is restored and decay heat removal is transitioned from the  
main steam safety valves to the #2 SG ADV for steam generator pressure control.  The  
inspectors noted that Dominion is currently implementing an unapproved OMA in lieu of  
inspectors noted that Dominion is currently implementing an unapproved OMA in lieu of  
meeting III.G.2 fire protection requirements.  Dominion promptly entered this safe  
meeting III.G.2 fire protection requirements.  Dominion promptly entered this safe  
shutdown issue into their corrective action program as CR 1043458.  Immediate corrective actions included implementing compensatory measures in the form of fire watches for fire area R-14 that are being tracked by RAS determination 3037040.   
shutdown issue into their corrective action program as CR 1043458.  Immediate  
 
corrective actions included implementing compensatory measures in the form of fire  
Longer term corrective actions included submitting an exemption request to the NRC for use of a local OMA to operate the #2 SG ADV in lieu of meeting fire protection  
watches for fire area R-14 that are being tracked by RAS determination 3037040.   
requirements for fire area R-14.  The team considered Dominion's immediate and longer term corrective actions appropriate.  
Longer term corrective actions included submitting an exemption request to the NRC for  
  Analysis:  Dominion's failure to protect the #2 SG ADV, credited for post-fire safe shutdown from fire damage in Fire Area R-14 caused by single spurious actuation, is  
use of a local OMA to operate the #2 SG ADV in lieu of meeting fire protection  
requirements for fire area R-14.  The team considered Dominions immediate and longer  
term corrective actions appropriate.  
   
Analysis:  Dominions failure to protect the #2 SG ADV, credited for post-fire safe  
shutdown from fire damage in Fire Area R-14 caused by single spurious actuation, is  
considered a performance deficiency.  The performance deficiency was more than minor  
considered a performance deficiency.  The performance deficiency was more than minor  
because it affected the Mitigating Systems cornerstone objective to ensure the availability, reliability, and capability of systems that respond to an external event to prevent undesirable consequences in the event of a fire.  Specifically, the use of an  
because it affected the Mitigating Systems cornerstone objective to ensure the  
availability, reliability, and capability of systems that respond to an external event to  
prevent undesirable consequences in the event of a fire.  Specifically, the use of an  
OMA during post-fire safe shutdown may not be as reliable as normal systems operation  
OMA during post-fire safe shutdown may not be as reliable as normal systems operation  
which could be utilized had the requirements of 10 CFR Part 50, Appendix R, Section   
which could be utilized had the requirements of 10 CFR Part 50, Appendix R, Section  
III.G.2 been met and, therefore, prevented fire damage to credited components and/or cables, specifically the #2 SG ADV.  
 
  The inspectors used IMC 0609, Appendix F, Fire Protection Significance Determination  
4
Process, Phase 1 and determined the reactor is able to reach and maintain a hot safe shutdown condition because the ADVs are used for transition to cold shutdown, therefore this finding was of very low safety significance (Green).  
  This finding does not have a cross cutting aspect because the performance deficiency  
   
occurred greater than three years ago when the June 30, 2011 exemption request letter to the NRC was supplemented by letter on February 29, 2012, and is not indicative of current licensee performance.   
III.G.2 been met and, therefore, prevented fire damage to credited components and/or  
  Enforcement:  Millstone Power Station, Unit 2, Renewed Facility Operating License Condition 2.C.(3) requires Dominion in part to implement and maintain in effect all  
cables, specifically the #2 SG ADV.  
provisions of the approved fire protection program as described in the FSAR.  FSAR Section 9.10.6, Safety Shutdown Design Bases, states in part Paragraph 50.48(b) of 10 CFR 50, which became effective on February 17, 1981, that all nuclear plants licensed  
   
The inspectors used IMC 0609, Appendix F, Fire Protection Significance Determination  
Process, Phase 1 and determined the reactor is able to reach and maintain a hot safe  
shutdown condition because the ADVs are used for transition to cold shutdown,  
therefore this finding was of very low safety significance (Green).  
   
This finding does not have a cross cutting aspect because the performance deficiency  
occurred greater than three years ago when the June 30, 2011 exemption request letter  
to the NRC was supplemented by letter on February 29, 2012, and is not indicative of  
current licensee performance.   
   
Enforcement:  Millstone Power Station, Unit 2, Renewed Facility Operating License  
Condition 2.C.(3) requires Dominion in part to implement and maintain in effect all  
provisions of the approved fire protection program as described in the FSAR.  FSAR  
Section 9.10.6, Safety Shutdown Design Bases, states in part Paragraph 50.48(b) of 10  
CFR 50, which became effective on February 17, 1981, that all nuclear plants licensed  
to operate prior to January 1, 1979, comply with specific portions of Section III of  
to operate prior to January 1, 1979, comply with specific portions of Section III of  
Appendix R to 10 CFR 50.  Section III.G requires that fire protection features be  
Appendix R to 10 CFR 50.  Section III.G requires that fire protection features be  
provided for those systems, structures, and components important to safe shutdown. These features must be capable of limiting fire damage so that one train of systems necessary to achieve and maintain hot shutdown conditions from either the main control  
provided for those systems, structures, and components important to safe shutdown.  
These features must be capable of limiting fire damage so that one train of systems  
necessary to achieve and maintain hot shutdown conditions from either the main control  
room or the emergency control stations is free of fire damage.   
room or the emergency control stations is free of fire damage.   
  Contrary to the above, since February 17, 1981 (the effective date of Appendix R and  
   
revised 10 CFR 50.48), and ongoing as of the inspection exit date, Dominion failed to implement all provisions of the approved fire protection program.  Specifically, the safe shutdown strategy in Fire Area R-14 for Millstone Unit 2 relied upon an unapproved  
Contrary to the above, since February 17, 1981 (the effective date of Appendix R and  
revised 10 CFR 50.48), and ongoing as of the inspection exit date, Dominion failed to  
implement all provisions of the approved fire protection program.  Specifically, the safe  
shutdown strategy in Fire Area R-14 for Millstone Unit 2 relied upon an unapproved  
OMA to mitigate post-fire safe shutdown equipment malfunctions caused by a single  
OMA to mitigate post-fire safe shutdown equipment malfunctions caused by a single  
spurious actuation, in lieu of protecting the equipment in accordance with 10 CFR Part  
spurious actuation, in lieu of protecting the equipment in accordance with 10 CFR Part  
50 Appendix R, Section III.G.2.  The specific OMA associated with Fire Area R-14 includes local manual control of the #2 SG ADV.  Dominion's immediate corrective actions included implementing compensatory measure in the form of fire watches for fire area R-14.  Because this violation was of very low safety significance (Green), and was  
50 Appendix R, Section III.G.2.  The specific OMA associated with Fire Area R-14  
entered into Dominion's CAP (CR 1043458), this issue is being treated as an NCV  
includes local manual control of the #2 SG ADV.  Dominions immediate corrective  
consistent with Section 2.3.2 of the Enforcement Policy.  (NCV 05000336/2016007-01, Unapproved OMA in Lieu of Meeting III.G.2 Fire Protection Requirements for Fire  
actions included implementing compensatory measure in the form of fire watches for fire  
Area R-14, Lower 4kV Switchgear Room and Cable Vault)
area R-14.  Because this violation was of very low safety significance (Green), and was  
  .02 Passive Fire Protection  
entered into Dominions CAP (CR 1043458), this issue is being treated as an NCV  
  a. Inspection Scope  
consistent with Section 2.3.2 of the Enforcement Policy.  (NCV 05000336/2016007-01,  
  The team walked down accessible portions of the selected fire areas to evaluate  
Unapproved OMA in Lieu of Meeting III.G.2 Fire Protection Requirements for Fire  
Area R-14, Lower 4kV Switchgear Room and Cable Vault)  
.02  
Passive Fire Protection  
   
a.  
Inspection Scope  
   
The team walked down accessible portions of the selected fire areas to evaluate  
whether the material conditions of the fire area boundaries were adequate for the fire  
whether the material conditions of the fire area boundaries were adequate for the fire  
hazards in the area.  The team compared the fire area boundaries, including walls,  
hazards in the area.  The team compared the fire area boundaries, including walls,  
ceilings, floors, fire doors, fire dampers, penetration seals, and redundant equipment fire   
ceilings, floors, fire doors, fire dampers, penetration seals, and redundant equipment fire  
barriers to design and licensing basis requirements, industry standards, and the Millstone Power Station Unit 2 and Unit 3 FPPs, as approved by the NRC, to identify any  
 
5
   
barriers to design and licensing basis requirements, industry standards, and the  
Millstone Power Station Unit 2 and Unit 3 FPPs, as approved by the NRC, to identify any  
potential degradation or non-conformances.  
potential degradation or non-conformances.  
  The team reviewed selected engineering evaluations, installation and repair work orders, and qualification records for a sample of penetration seals to determine whether the fill material was properly installed and whether the as-left configuration satisfied design requirements for the intended fire rating.   
   
  The team also reviewed recent inspection and functional test records for fire dampers, and the inspection records for penetration seals and fire barriers, to verify whether the inspection and testing was adequately conducted, the acceptance criteria were met, and  
The team reviewed selected engineering evaluations, installation and repair work orders,  
and qualification records for a sample of penetration seals to determine whether the fill  
material was properly installed and whether the as-left configuration satisfied design  
requirements for the intended fire rating.   
   
The team also reviewed recent inspection and functional test records for fire dampers,  
and the inspection records for penetration seals and fire barriers, to verify whether the  
inspection and testing was adequately conducted, the acceptance criteria were met, and  
any potential performance degradation was identified.  
any potential performance degradation was identified.  
 
  b. Findings  
  b.  
  No findings were identified.  
Findings  
   .03 Active Fire Protection
   
    a. Inspection Scope  
No findings were identified.  
  The team evaluated manual and automatic fire suppression and detection systems in the  
    
.03  
Active Fire Protection  
  a.  
Inspection Scope  
   
The team evaluated manual and automatic fire suppression and detection systems in the  
selected fire areas to determine whether they were installed, tested, maintained, and  
selected fire areas to determine whether they were installed, tested, maintained, and  
operated in accordance with NRC requirements, National Fire Protection Association  
operated in accordance with NRC requirements, National Fire Protection Association  
(NFPA) codes of record, and the Millstone  
(NFPA) codes of record, and the Millstone FPPs, as approved by the NRC.  The team  
FPPs, as approved by the NRC.  The team also assessed whether the suppression systems capabilities were adequate to control and/or extinguish fires associated with the hazards in the selected areas.  
also assessed whether the suppression systems capabilities were adequate to control  
  The team reviewed the as-built capability of the fire water supply system to verify the design and licensing basis and NFPA code of record requirements were satisfied, and to  
and/or extinguish fires associated with the hazards in the selected areas.  
   
The team reviewed the as-built capability of the fire water supply system to verify the  
design and licensing basis and NFPA code of record requirements were satisfied, and to  
assess whether those capabilities were adequate for the hazards involved.  The team  
assess whether those capabilities were adequate for the hazards involved.  The team  
reviewed the fire water system hydraulic analyses to assess the adequacy of a single fire water pump to supply the largest single hydraulic load on the fire water system plus  
reviewed the fire water system hydraulic analyses to assess the adequacy of a single  
fire water pump to supply the largest single hydraulic load on the fire water system plus  
concurrent fire hose usage.  The team evaluated the fire pump performance tests to  
concurrent fire hose usage.  The team evaluated the fire pump performance tests to  
assess the adequacy of the test acceptance criteria for pump minimum discharge  
assess the adequacy of the test acceptance criteria for pump minimum discharge  
pressure at the required flow rate, to verify the criteria was adequate to ensure that the design basis and hydraulic analysis requirements were satisfied.  The team also evaluated the underground fire loop flow tests to verify the tests adequately  
pressure at the required flow rate, to verify the criteria was adequate to ensure that the  
design basis and hydraulic analysis requirements were satisfied.  The team also  
evaluated the underground fire loop flow tests to verify the tests adequately  
demonstrated that the flow distribution circuits were able to meet design basis  
demonstrated that the flow distribution circuits were able to meet design basis  
requirements.  In addition, the team reviewed recent pump and loop flow test results to  
requirements.  In addition, the team reviewed recent pump and loop flow test results to  
verify the testing was adequately conducted, the acceptance criteria were met, and any  
verify the testing was adequately conducted, the acceptance criteria were met, and any  
potential performance degradation was identified.  
potential performance degradation was identified.  
  The team reviewed initial discharge testing, design specifications, vendor requirements, modifications and engineering evaluations, and routine functional testing for the CO
   
2 and Halon suppression systems for the areas protection.  The team walked down accessible  
The team reviewed initial discharge testing, design specifications, vendor requirements,  
potions of the CO
modifications and engineering evaluations, and routine functional testing for the CO2 and
2 and Halon systems, including storage tanks and supply systems, to
Halon suppression systems for the areas protection.  The team walked down accessible  
6  independently assess the material condition, operational lineup, and availability of the systems.  The team also reviewed and walked down the associated firefighting
potions of the CO2 and Halon systems, including storage tanks and supply systems, to  
strategies and CO
2 and Halon system operating procedures. 
The team walked down accessible portions of the detection and water suppression systems in the selected areas and major portions of the fire water supply system, including motor and diesel driven fire
pumps, interviewed system and program engineers, and reviewed selected correct
ive action program documents (condition reports) to independently assess the material condition of the systems and components.  In addition, the team reviewed recent test results for the fire detection and suppression systems for the selected fire areas to verify the testing was adequately conducted, the acceptance criteria were met, and any performance degradation was identified. 


6
independently assess the material condition, operational lineup, and availability of the
systems.  The team also reviewed and walked down the associated firefighting
strategies and CO2 and Halon system operating procedures. 
The team walked down accessible portions of the detection and water suppression
systems in the selected areas and major portions of the fire water supply system,
including motor and diesel driven fire pumps, interviewed system and program
engineers, and reviewed selected corrective action program documents (condition
reports) to independently assess the material condition of the systems and components. 
In addition, the team reviewed recent test results for the fire detection and suppression
systems for the selected fire areas to verify the testing was adequately conducted, the
acceptance criteria were met, and any performance degradation was identified. 
   
   
The team assessed the fire brigade capabilities by reviewing training, qualification, and  
The team assessed the fire brigade capabilities by reviewing training, qualification, and  
drill critique records.  The team also reviewed Millstone's firefighting strategies (i.e. pre-
drill critique records.  The team also reviewed Millstone's firefighting strategies (i.e. pre-
fire plans) and smoke removal plans for the selected fire areas to determine if appropriate information was provided to fire brigade members and plant operators to identify safe shutdown equipment and instrumentation, and to facilitate suppression of a  
fire plans) and smoke removal plans for the selected fire areas to determine if  
appropriate information was provided to fire brigade members and plant operators to  
identify safe shutdown equipment and instrumentation, and to facilitate suppression of a  
fire that could impact post-fire safe shutdown capability.  The team independently  
fire that could impact post-fire safe shutdown capability.  The team independently  
inspected the fire brigade equipment, including personnel protective gear (e.g. turnout  
inspected the fire brigade equipment, including personnel protective gear (e.g. turnout  
gear) and smoke removal equipment, to determine operational readiness for firefighting.  In addition, the team reviewed Millstone's fire brigade equipment inventory and inspection procedure and recent inspection and inventory results to verify adequate  
gear) and smoke removal equipment, to determine operational readiness for firefighting.   
In addition, the team reviewed Millstone's fire brigade equipment inventory and  
inspection procedure and recent inspection and inventory results to verify adequate  
equipment was available, and any potential material deficiencies were identified.  
equipment was available, and any potential material deficiencies were identified.  
   
   
   b.  Findings  
   b.   
  No findings were identified.  
Findings  
   
No findings were identified.  
.04
Protection from Damage from Fire Suppression Activities
   
   
.04 Protection from Damage from Fire Suppression Activities
  a.  
Inspection Scope
   
   
  a. Inspection Scope
The team walked down the selected fire areas and adjacent areas, and reviewed  
The team walked down the selected fire areas and adjacent areas, and reviewed  
selected documents to determine whether redundant safe shutdown trains could be  
selected documents to determine whether redundant safe shutdown trains could be  
potentially damaged from fire suppression activi
potentially damaged from fire suppression activities or from the rupture or inadvertent  
ties or from the rupture or inadvertent operation of fire suppression systems.  During the walkdowns, the team evaluated the adequacy and condition of floor drains, equipment elevations, and spray protection.   
operation of fire suppression systems.  During the walkdowns, the team evaluated the  
Specifically, to determine whether a potential existed to damage redundant safe shutdown trains, the team evaluated whether:  
adequacy and condition of floor drains, equipment elevations, and spray protection.   
  A fire in one of the selected fire areas would not release smoke, heat, or hot gases that could cause unintended activation of suppression systems in adjacent fire areas which could potentially damage all redundant safe shutdown trains; or  
Specifically, to determine whether a potential existed to damage redundant safe  
  A fire suppression system rupture, inadvertent actuation, or actuation due to a fire, in one of the selected fire areas, could not directly damage all redundant trains (e.g. sprinkler caused flooding of other than the locally affected train); and   
shutdown trains, the team evaluated whether:  
7    Adequate drainage was provided in areas protected by water suppression systems.   
   b. Findings  
  No findings were identified.   
A fire in one of the selected fire areas would not release smoke, heat, or hot  
  .05 Post-Fire Safe Shutdown Capability - Normal and Alternative
gases that could cause unintended activation of suppression systems in adjacent  
    a.  Inspection Scope  
fire areas which could potentially damage all redundant safe shutdown trains; or  
  The team reviewed the safe shutdown analysis, thermal-hydraulic analysis, operating procedures, time critical operator action validation studies, piping and instrumentation  
A fire suppression system rupture, inadvertent actuation, or actuation due to a  
fire, in one of the selected fire areas, could not directly damage all redundant  
trains (e.g. sprinkler caused flooding of other than the locally affected train); and  
 
7
   
Adequate drainage was provided in areas protected by water suppression  
systems.  
   
   b.  
Findings  
   
No findings were identified.   
   
.05  
Post-Fire Safe Shutdown Capability - Normal and Alternative  
  a.   
Inspection Scope  
   
The team reviewed the safe shutdown analysis, thermal-hydraulic analysis, operating  
procedures, time critical operator action validation studies, piping and instrumentation  
drawings (P&lDs), electrical drawings, the UFSAR, and other supporting documents for  
drawings (P&lDs), electrical drawings, the UFSAR, and other supporting documents for  
the selected fire areas to verify whether Dominion had properly identified the systems  
the selected fire areas to verify whether Dominion had properly identified the systems  
and components necessary to achieve and maintain post-fire safe shutdown conditions.   
and components necessary to achieve and maintain post-fire safe shutdown conditions.   
The team evaluated selected systems and co
The team evaluated selected systems and components credited by the safe shutdown  
mponents credited by the safe shutdown analysis for reactor pressure control, reactivity control, reactor coolant makeup, decay heat removal, process monitoring, and support system functions to assess the adequacy  
analysis for reactor pressure control, reactivity control, reactor coolant makeup, decay  
heat removal, process monitoring, and support system functions to assess the adequacy  
of Dominion's alternative shutdown methodology.  The team also assessed whether  
of Dominion's alternative shutdown methodology.  The team also assessed whether  
alternative post-fire shutdown could be perfo
alternative post-fire shutdown could be performed both with and without the availability  
rmed both with and without the availability of off-site power.  The team walked down selected plant configurations to verify whether they were consistent with the assumptions and descriptions in the safe shutdown and fire hazards analyses.  In addition, the team evaluated whether the systems and  
of off-site power.  The team walked down selected plant configurations to verify whether  
they were consistent with the assumptions and descriptions in the safe shutdown and  
fire hazards analyses.  In addition, the team evaluated whether the systems and  
components credited for use during post-fire safe shutdown would remain free from fire  
components credited for use during post-fire safe shutdown would remain free from fire  
damage.   
damage.   
 
The team reviewed the training program for licensed and non-licensed operators to verify whether it included alternative shutdown capability.  The team also verified  
The team reviewed the training program for licensed and non-licensed operators to  
verify whether it included alternative shutdown capability.  The team also verified  
whether personnel required for post-fire safe shutdown, using either the normal or  
whether personnel required for post-fire safe shutdown, using either the normal or  
alternative shutdown methods, were trained and available on-site at all times, exclusive of those assigned as fire brigade members.  
alternative shutdown methods, were trained and available on-site at all times, exclusive  
 
of those assigned as fire brigade members.  
The team reviewed the adequacy of procedures utilized for post-fire shutdown and performed an independent walk through of procedure steps (i.e., a procedure tabletop)  
The team reviewed the adequacy of procedures utilized for post-fire shutdown and  
performed an independent walk through of procedure steps (i.e., a procedure tabletop)  
to assess the adequacy of implementation and human factors within the procedures.   
to assess the adequacy of implementation and human factors within the procedures.   
The team also evaluated the time required to perform specific actions to verify whether  
The team also evaluated the time required to perform specific actions to verify whether  
operators could reasonably be expected to perform those actions within sufficient time to maintain plant parameters within specified limits.   
operators could reasonably be expected to perform those actions within sufficient time to  
  Specific procedures reviewed for normal and alternative post-fire shutdown included the  
maintain plant parameters within specified limits.   
 
   
Specific procedures reviewed for normal and alternative post-fire shutdown included the  
following:  
following:  
Unit 2
AOP 2559, Fire;
AOP 2579A, Fire Procedure for Hot Standby Appendix R Fire Area R-1;


  Unit 2  AOP 2559, Fire; AOP 2579A, Fire Procedure for Hot Standby Appendix R Fire Area R-1;  
8
8    AOP 2579AA, Fire Procedure for Cooldown and Cold Shutdown Appendix R Fire  
   
Area R-1;  AOP 2579EE, Fire Procedure for Cooldown and Cold Shutdown Appendix R Fire  
   
Area R-7, R-9, R-14, and R-17;  AOP 2579G, Fire Procedure for Hot Standby Appendix R Fire Area R-7; and,  AOP 2579M, Fire Procedure for Hot Standby Appendix R Fire Area R-14.  
   
  Unit 3   EOP 3509, Fire Emergency;  EOP 3509.1, Control Room, Cable Spreading Area or Instrument Rack Room  
AOP 2579AA, Fire Procedure for Cooldown and Cold Shutdown Appendix R Fire  
Fire;   EOP 3509.6, Auxiliary Building West MCC/Rod Control/ACU Area Fire;  EOP 3509.15, North (A) EDG Enclosure or East (A) F.O. Vault Fire; and,   EOP 3509.19, ESF Building North RHR Heat Exchanger Cubicle Fire.  
Area R-1;  
  The team reviewed selected operator manual actions to verify whether they had been properly reviewed and approved and whether the actions could be implemented in accordance with plant procedures in the time necessary to support the safe shutdown  
   
AOP 2579EE, Fire Procedure for Cooldown and Cold Shutdown Appendix R Fire  
Area R-7, R-9, R-14, and R-17;  
   
AOP 2579G, Fire Procedure for Hot Standby Appendix R Fire Area R-7; and,  
   
AOP 2579M, Fire Procedure for Hot Standby Appendix R Fire Area R-14.  
   
Unit 3  
EOP 3509, Fire Emergency;  
   
EOP 3509.1, Control Room, Cable Spreading Area or Instrument Rack Room  
Fire;
EOP 3509.6, Auxiliary Building West MCC/Rod Control/ACU Area Fire;  
   
EOP 3509.15, North (A) EDG Enclosure or East (A) F.O. Vault Fire; and,
EOP 3509.19, ESF Building North RHR Heat Exchanger Cubicle Fire.  
   
The team reviewed selected operator manual actions to verify whether they had been  
properly reviewed and approved and whether the actions could be implemented in  
accordance with plant procedures in the time necessary to support the safe shutdown  
method for each fire area.  The team also reviewed the periodic testing of the alternative  
method for each fire area.  The team also reviewed the periodic testing of the alternative  
shutdown transfer and isolation capability, and instrumentation and control functions, to  
shutdown transfer and isolation capability, and instrumentation and control functions, to  
evaluate whether the tests were adequate to ensure the functionality of the alternative  
evaluate whether the tests were adequate to ensure the functionality of the alternative  
shutdown capability.  
shutdown capability.  
b. Findings
No findings were identified.
    .06 Circuit Analysis
   
   
  a. Inspection Scope 
b.  
  The team verified that the licensee performed a post-fire safe shutdown analysis for the selected fire areas and the analysis appropriately identified the structures, systems, and components important to achieving and maintaining safe shutdown.  Additionally, the
Findings
team verified that the licensee's analysis ensured that necessary electrical circuits were properly protected and that circuits that could adversely impact safe shutdown due to hot
   
shorts or shorts to ground were identified, evaluated, and dispositioned to ensure spurious actuations would not prevent safe shutdown.  
No findings were identified.  
   
   
The team's review considered fire and cable attributes, cable routing, potential  
.06
Circuit Analysis
  a.
Inspection Scope 
The team verified that the licensee performed a post-fire safe shutdown analysis for the
selected fire areas and the analysis appropriately identified the structures, systems, and
components important to achieving and maintaining safe shutdown.  Additionally, the
team verified that the licensees analysis ensured that necessary electrical circuits were
properly protected and that circuits that could adversely impact safe shutdown due to hot
shorts or shorts to ground were identified, evaluated, and dispositioned to ensure
spurious actuations would not prevent safe shutdown.
The teams review considered fire and cable attributes, cable routing, potential  
undesirable consequences and common power supply/bus concerns.  Specific items  
undesirable consequences and common power supply/bus concerns.  Specific items  
included the credibility of the fire threat, cable insulation attributes, cable failure modes,  
included the credibility of the fire threat, cable insulation attributes, cable failure modes,  
and actuations resulting in flow diversion or loss of coolant events.  
and actuations resulting in flow diversion or loss of coolant events.  
  The team also reviewed cable raceway drawings and/or cable routing databases for a  
   
sample of components required for post-fire safe shutdown to verify that cables were   
The team also reviewed cable raceway drawings and/or cable routing databases for a  
routed as described in the safe shutdown analysis.  The team also reviewed equipment important to safe shutdown, but not part of the success path, to verify that the licensee  
sample of components required for post-fire safe shutdown to verify that cables were  
 
9
   
routed as described in the safe shutdown analysis.  The team also reviewed equipment  
important to safe shutdown, but not part of the success path, to verify that the licensee  
had taken appropriate actions in accordance with the design and licensing basis and  
had taken appropriate actions in accordance with the design and licensing basis and  
NRC Regulatory Guide 1.189, Revision 2.  
NRC Regulatory Guide 1.189, Revision 2.  
 
Cable failure modes were reviewed for the following components:  
Cable failure modes were reviewed for the following components:  
  Unit 2   P18B, Charging Pump 'B';  2-CH-501, VCT Outlet Header to Charging Pumps Isolation Valve;  2-CH-519, Loop 1A Charging Isolation Valve; and,  PI-1023B-1, SG #2 Pressure Indicator.  
   
  Unit 3   3RCS*LCV459, VCT Letdown Isolation Valve;  3RCS*SV8095A, Head Vent Isolation Valve;  3CHS*MV8438A, Charging Pump 'A' Header Isolation Valve;  3FWS*LI501A, SG #1 Level Indicator; and,  3RCS*PI405B, RCS Pressure Indicator.  
Unit 2  
  The team reviewed a sample of circuit breaker coordination studies to ensure equipment  
P18B, Charging Pump B;  
   
2-CH-501, VCT Outlet Header to Charging Pumps Isolation Valve;  
   
2-CH-519, Loop 1A Charging Isolation Valve; and,  
   
PI-1023B-1, SG #2 Pressure Indicator.  
   
Unit 3  
3RCS*LCV459, VCT Letdown Isolation Valve;  
   
3RCS*SV8095A, Head Vent Isolation Valve;  
   
3CHS*MV8438A, Charging Pump A Header Isolation Valve;  
   
3FWS*LI501A, SG #1 Level Indicator; and,  
   
3RCS*PI405B, RCS Pressure Indicator.  
   
The team reviewed a sample of circuit breaker coordination studies to ensure equipment  
needed to conduct post-fire safe shutdown activities would not be impacted due to a lack  
needed to conduct post-fire safe shutdown activities would not be impacted due to a lack  
of coordination that could result in a common power supply or common bus concern.   
of coordination that could result in a common power supply or common bus concern.   
  The team verified that the transfer of control from the control room to the alternative  
   
The team verified that the transfer of control from the control room to the alternative  
shutdown location(s) would not be affected by fire-induced circuit faults (e.g. by the  
shutdown location(s) would not be affected by fire-induced circuit faults (e.g. by the  
provision of separate fuses and power supplies for alternative shutdown control circuits).  
provision of separate fuses and power supplies for alternative shutdown control circuits).  
    b. Findings  
 
  No findings were identified.  
  b.  
 
Findings  
.07 Communications
   
    a. Inspection Scope   
No findings were identified.  
  The team reviewed safe shutdown procedures, the safe shutdown analysis, and  
.07  
Communications  
  a.  
Inspection Scope   
   
The team reviewed safe shutdown procedures, the safe shutdown analysis, and  
associated documents to verify an adequate method of communications would be  
associated documents to verify an adequate method of communications would be  
available to plant operators following a fire.  During this review the team considered the effects of ambient noise levels, clarity of reception, reliability, and coverage patterns.  The team also inspected the designated emergency storage lockers to verify the  
available to plant operators following a fire.  During this review the team considered the  
effects of ambient noise levels, clarity of reception, reliability, and coverage patterns.   
The team also inspected the designated emergency storage lockers to verify the  
availability of portable radios for the fire brigade and for plant operators.  The team also  
availability of portable radios for the fire brigade and for plant operators.  The team also  
verified that communications equipment such as repeaters and transmitters would not be  
verified that communications equipment such as repeaters and transmitters would not be  
affected by a fire.  
affected by a fire.  
   
10    b. Findings
No findings were identified.
   
   
.08 Emergency Lighting
   
   
   a. Inspection Scope  
  The team observed the placement and coverage area of eight-hour emergency lights  
 
throughout the selected fire areas to evaluate their adequacy for illuminating access and egress pathways and any equipment requiring local operation or instrumentation monitoring for post-fire safe shutdown.  The team also verified that the battery power  
10
  b.
Findings
No findings were identified.
.08
Emergency Lighting
   a.  
Inspection Scope  
   
The team observed the placement and coverage area of eight-hour emergency lights  
throughout the selected fire areas to evaluate their adequacy for illuminating access and  
egress pathways and any equipment requiring local operation or instrumentation  
monitoring for post-fire safe shutdown.  The team also verified that the battery power  
supplies were rated for at least an eight-hour capacity.  Preventive maintenance  
supplies were rated for at least an eight-hour capacity.  Preventive maintenance  
procedures, the vendor manual, completed surveillance tests, and battery replacement  
procedures, the vendor manual, completed surveillance tests, and battery replacement  
practices were also reviewed to verify that the emergency lighting was being maintained  
practices were also reviewed to verify that the emergency lighting was being maintained  
consistent with the manufacturer's recommendations and in a manner that would ensure reliable operation.  
consistent with the manufacturers recommendations and in a manner that would ensure  
  b. Findings  
reliable operation.  
  No findings were identified.  
   
  .09 Cold Shutdown Repairs  
b.  
Findings  
   
No findings were identified.  
   
.09  
Cold Shutdown Repairs  
  a.
Inspection Scope
   
   
  a. Inspection Scope
The team reviewed Dominion's dedicated repair procedures, for components which  
The team reviewed Dominion's dedicated repair procedures, for components which might be damaged by fire and were required to achieve post-fire cold shutdown (CSD).  The team evaluated selected CSD repairs to determine whether they could be achieved  
might be damaged by fire and were required to achieve post-fire cold shutdown (CSD).   
The team evaluated selected CSD repairs to determine whether they could be achieved  
within the time frames assumed in the design and licensing bases.  In addition, the team  
within the time frames assumed in the design and licensing bases.  In addition, the team  
verified whether the necessary repair equipment, tools, and materials (e.g., pre-cut  
verified whether the necessary repair equipment, tools, and materials (e.g., pre-cut  
cables with prepared attachment lugs) were available and accessible on site.   
cables with prepared attachment lugs) were available and accessible on site.   
  b. Findings  
  b.  
Findings  
   
   
No findings were identified.  
No findings were identified.  
 
.10 Compensatory Measures
.10  
    a. Inspection Scope  
Compensatory Measures  
  a.  
Inspection Scope  
   
   
The team verified compensatory measures were in place for out-of-service, degraded, or  
The team verified compensatory measures were in place for out-of-service, degraded, or  
inoperable fire protection and post-fire safe shutdown equipment, systems, or features (e.g., detection and suppression systems and equipment, passive fire barriers, pumps, valves, or electrical devices providing safe shutdown functions or capabilities).  The team evaluated whether the short term compensatory measures adequately  
inoperable fire protection and post-fire safe shutdown equipment, systems, or features  
compensated for the degraded function or feature until appropriate corrective action
(e.g., detection and suppression systems and equipment, passive fire barriers, pumps,  
11  could be taken and that the licensee was effective in returning the equipment to service in a reasonable period of time.
valves, or electrical devices providing safe shutdown functions or capabilities).  The  
team evaluated whether the short term compensatory measures adequately  
compensated for the degraded function or feature until appropriate corrective action  


  b. Findings   
11
  No findings were identified.  
could be taken and that the licensee was effective in returning the equipment to service
in a reasonable period of time.
  b.  
Findings   
   
No findings were identified.  
.11
Fire Protection Program Changes
  a.
Inspection Scope
   
   
.11 Fire Protection Program Changes
The team reviewed recent changes to the approved fire protection program to verify that  
    a. Inspection Scope
The team reviewed recent changes to the approved fire protection program to verify that  
the changes did not constitute an adverse effect on the ability to safely shutdown.  
the changes did not constitute an adverse effect on the ability to safely shutdown.  
   
   
   b. Findings   
   b.  
  No findings were identified.  
Findings   
   
No findings were identified.  
.12
Control of Transient Combustibles and Ignition Sources
  a.
Inspection Scope
   
   
.12 Control of Transient Combustibles and Ignition Sources
The team reviewed the licensees procedures and programs for the control of ignition  
    a. Inspection Scope
The team reviewed the licensee's procedures and programs for the control of ignition  
sources and transient combustibles to assess their effectiveness in preventing fires and  
sources and transient combustibles to assess their effectiveness in preventing fires and  
in controlling combustible loading within limits established in the FHA.  A sample of hot work and transient combustible control permits were also reviewed.  The team  
in controlling combustible loading within limits established in the FHA.  A sample of hot  
performed plant walkdowns to verify that transient combustibles and ignition sources were being implemented in accordance with the administrative controls.  
work and transient combustible control permits were also reviewed.  The team  
  b. Findings   
performed plant walkdowns to verify that transient combustibles and ignition sources  
  No findings were identified.  
were being implemented in accordance with the administrative controls.  
  .13 Large Fires and Explosions Mitigation Strategies
    a. Inspection Scope  
  b.  
  The team conducted a review of selected mitigation strategies intended to maintain or restore core decay heat removal and spent fuel pool cooling capabilities under the  
Findings   
   
No findings were identified.  
   
.13  
Large Fires and Explosions Mitigation Strategies  
  a.  
Inspection Scope  
   
The team conducted a review of selected mitigation strategies intended to maintain or  
restore core decay heat removal and spent fuel pool cooling capabilities under the  
circumstances associated with the loss of large areas of the plant due to explosions  
circumstances associated with the loss of large areas of the plant due to explosions  
and/or fires.  The team assessed whether Dominion continued to meet the requirements  
and/or fires.  The team assessed whether Dominion continued to meet the requirements  
of the Millstone Power Station Units 2 and 3 Operating Licenses and 10 CFR  
of the Millstone Power Station Units 2 and 3 Operating Licenses and 10 CFR  
50.54(hh)(2).   
50.54(hh)(2).   
  The team reviewed the following mitigation strategies:  
   
The team reviewed the following mitigation strategies:  
Unit 2 and 3 Manual Operation of Turbine-Driven AFW Pump; and,
Unit 2 and 3 Manual Operation of SG ADVs.


  Unit 2 and 3 Manual Operation of Turbine-Driven AFW Pump; and, Unit 2 and 3 Manual Operation of SG ADVs.  
12
12    The team's review included:  a detailed assessment of the procedural guidance; a  
   
   
The team's review included:  a detailed assessment of the procedural guidance; a  
tabletop discussion with licensed operators; and a walk down of four mitigation  
tabletop discussion with licensed operators; and a walk down of four mitigation  
strategies with operators to assess the feasibility of the strategies and operator  
strategies with operators to assess the feasibility of the strategies and operator  
familiarity; maintenance and surveillance testing of selected strategy equipment; and an inventory check of the B.5.b pump and equipment trailers to ensure the appropriateness of equipment storage and availability.  
familiarity; maintenance and surveillance testing of selected strategy equipment; and an  
 
inventory check of the B.5.b pump and equipment trailers to ensure the appropriateness  
  b. Findings  
of equipment storage and availability.  
  No findings were identified.  
  4. OTHER ACTIVITIES [OA]  
  b.  
  4OA2 Identification and Resolution of Problems (IP 71152)
Findings  
  .01 Corrective Actions for Fire Protection Deficiencies  
   
No findings were identified.  
   
4.  
OTHER ACTIVITIES [OA]  
   
4OA2 Identification and Resolution of Problems (IP 71152)  
.01  
Corrective Actions for Fire Protection Deficiencies  
  a.
Inspection Scope
   
   
  a. Inspection Scope
The team reviewed a sample of condition reports associated with fire protection program  
The team reviewed a sample of condition reports associated with fire protection program and post-fire safe shutdown issues to determine whether Millstone was appropriately identifying, characterizing, and correcting problems in these areas, and to assess  
and post-fire safe shutdown issues to determine whether Millstone was appropriately  
identifying, characterizing, and correcting problems in these areas, and to assess  
whether the planned or completed corrective actions were appropriate.  
whether the planned or completed corrective actions were appropriate.  
   
   
   b. Findings   
   b.  
  No findings were identified.   
Findings   
   
No findings were identified.   
4OA3 Follow-up of Events and Notices of Enforcement Discretion (IP 71153)
.1
(Closed) Licensee Event Report (LER) 05000336/2013-003-00 (Unit 2):  Postulated DC
Ammeter Circuit Hot Shorts
   
   
4OA3 Follow-up of Events and Notices of Enforcement Discretion (IP 71153)
On October 30, 2013, during a review of industry operating experience, Dominion  
  .1 (Closed) Licensee Event Report (LER) 05000336/2013-003-00 (Unit 2):  Postulated DC Ammeter Circuit Hot Shorts
On October 30, 2013, during a review of industry operating experience, Dominion  
identified a postulated fire induced circuit failure involving unfused direct current (DC)  
identified a postulated fire induced circuit failure involving unfused direct current (DC)  
ammeter circuits for Millstone Power Station, Unit 2.  The fire induced circuit failures could cause a secondary fire that could adversely affect safe shutdown equipment and cause a loss of alternate shutdown capability which is contrary to Unit 2 Renewed  
ammeter circuits for Millstone Power Station, Unit 2.  The fire induced circuit failures  
could cause a secondary fire that could adversely affect safe shutdown equipment and  
cause a loss of alternate shutdown capability which is contrary to Unit 2 Renewed  
Facility Operating License Condition 2.C.(3) and Appendix R requirements.  The license  
Facility Operating License Condition 2.C.(3) and Appendix R requirements.  The license  
condition and regulation requires in part, post-fire safe shutdown cables remain free of  
condition and regulation requires in part, post-fire safe shutdown cables remain free of  
the effects of fire-induced cable faults during postulated fires.  Specifically, the licensee  
the effects of fire-induced cable faults during postulated fires.  Specifically, the licensee  
identified DC ammeter circuits for Unit 2, were not provided with overcurrent protection to limit fault current in the 125 volt (V) DC systems.  Postulated fires that result in a short to ground concurrent with an opposite polarity short from the same battery could result in  
identified DC ammeter circuits for Unit 2, were not provided with overcurrent protection  
to limit fault current in the 125 volt (V) DC systems.  Postulated fires that result in a short  
to ground concurrent with an opposite polarity short from the same battery could result in  
excessive current flow in the ammeter wiring.  The excessive current could heat-up the  
excessive current flow in the ammeter wiring.  The excessive current could heat-up the  
conductor and could result in a secondary fire in another fire area.  The secondary fire  
conductor and could result in a secondary fire in another fire area.  The secondary fire  
could adversely affect safe shutdown equipment and cause a loss of alternate shutdown   
could adversely affect safe shutdown equipment and cause a loss of alternate shutdown  
13  capability.  Dominion determined the cause of the condition was a latent design error that was made during plant construction involving the failure to include protective fuses  
 
13
   
capability.  Dominion determined the cause of the condition was a latent design error  
that was made during plant construction involving the failure to include protective fuses  
in DC ammeter circuits.  
in DC ammeter circuits.  
   
   
The licensee submitted LER 05000336/2013-003-00 to report this event in accordance with 10 CFR 50.73(a)(2)(ii)(B) as an unanalyzed condition that significantly degraded plant safety.  The licensee entered this issue into their corrective action program as condition report number CR530987 and implemented compensatory measures in the  
The licensee submitted LER 05000336/2013-003-00 to report this event in accordance  
with 10 CFR 50.73(a)(2)(ii)(B) as an unanalyzed condition that significantly degraded  
plant safety.  The licensee entered this issue into their corrective action program as  
condition report number CR530987 and implemented compensatory measures in the  
affected fire areas pending final resolution of the issue.  
affected fire areas pending final resolution of the issue.  
  The licensee completed an engineering evaluation (RAS000244) of the issue and developed a design change (MP2-14-01007) to add fuses to the affected ammeter  
   
The licensee completed an engineering evaluation (RAS000244) of the issue and  
developed a design change (MP2-14-01007) to add fuses to the affected ammeter  
circuits.  Dominion completed the necessary modifications for all affected ammeter  
circuits.  Dominion completed the necessary modifications for all affected ammeter  
circuits by May 7, 2014.  
circuits by May 7, 2014.  
The significance and enforcement aspect of this issue are discussed in Section 4OA7.1 of this inspection report.  LER 05000336/2013-003-00 is closed.
   
   
.2 (Closed) Licensee Event Report (LER) 05000336/2014-002-00 (Unit 2):  DC Circuit Hot  
The significance and enforcement aspect of this issue are discussed in Section 4OA7.1
Shorts  On March 12, 2014, during a review of industry operating experience, Dominion identified postulated fire induced circuit failures involving unfused DC motor control  
of this inspection report.  LER 05000336/2013-003-00 is closed.
circuits for Millstone Power Station Unit 2.  The postulated fire induced circuit failures could cause a secondary fire that could adversely affect fire safe shutdown equipment  
contrary to Unit 2 Renewed Facility Operating License Condition 2.C.(3) and Appendix R requirements.  The license condition and regulation requires in part, post-fire safe shutdown cables remain free of the effects of fire induced cable faults during postulated fires.  Specifically, the licensee identified 125 V DC control and indication circuits for a  
.2  
non-safety related main turbine emergency lube oil pump that was not provided with overcurrent protection.  Postulated fires in the turbine battery room, the cable vault, the  
(Closed) Licensee Event Report (LER) 05000336/2014-002-00 (Unit 2):  DC Circuit Hot  
plant equipment operator meeting area and the control room could cause failure of the unprotected 125 V DC circuits, which in turn could cause failure of the control circuits for safe shutdown equipment.  Dominion determined the cause of the condition was a  
Shorts  
manufacturer's design error that involved the failure to include protective fuses in DC  
   
On March 12, 2014, during a review of industry operating experience, Dominion  
identified postulated fire induced circuit failures involving unfused DC motor control  
circuits for Millstone Power Station Unit 2.  The postulated fire induced circuit failures  
could cause a secondary fire that could adversely affect fire safe shutdown equipment  
contrary to Unit 2 Renewed Facility Operating License Condition 2.C.(3) and Appendix  
R requirements.  The license condition and regulation requires in part, post-fire safe  
shutdown cables remain free of the effects of fire induced cable faults during postulated  
fires.  Specifically, the licensee identified 125 V DC control and indication circuits for a  
non-safety related main turbine emergency lube oil pump that was not provided with  
overcurrent protection.  Postulated fires in the turbine battery room, the cable vault, the  
plant equipment operator meeting area and the control room could cause failure of the  
unprotected 125 V DC circuits, which in turn could cause failure of the control circuits for  
safe shutdown equipment.  Dominion determined the cause of the condition was a  
manufacturers design error that involved the failure to include protective fuses in DC  
motor control circuits during plant construction.  
motor control circuits during plant construction.  
  The licensee submitted LER 05000336/2014-002-00 (Unit 2) to report this event in accordance with 10 CFR 50.73(a)(2)(ii)(B) as an unanalyzed condition that significantly degraded plant safety.  The licensee entered this issue into their corrective action  
   
program as condition report number CR541980 and implemented compensatory measures in the affected fire areas pending final resolution of the issue.  
The licensee submitted LER 05000336/2014-002-00 (Unit 2) to report this event in  
accordance with 10 CFR 50.73(a)(2)(ii)(B) as an unanalyzed condition that significantly  
degraded plant safety.  The licensee entered this issue into their corrective action  
program as condition report number CR541980 and implemented compensatory  
measures in the affected fire areas pending final resolution of the issue.  
   
   
The licensee completed an engineering evaluation (RAS000252) of the issue and  
The licensee completed an engineering evaluation (RAS000252) of the issue and  
Line 512: Line 1,053:
the affected motor control circuit.  Dominion completed the necessary modifications for  
the affected motor control circuit.  Dominion completed the necessary modifications for  
the affected motor control circuit by May 5, 2014.  
the affected motor control circuit by May 5, 2014.  
 
14  The significance and enforcement aspect of this issue are discussed in Section 4OA7.2 of this inspection report.  LER 05000336/2014-002-00 (Unit 2) is closed.
   
   
.3 (Closed) Licensee Event Report (LER) 05000423/2014-002-00 (Unit 3):  DC Circuit Hot  
 
Shorts  On March 12, 2014, during a review of industry operating experience, Dominion identified postulated fire induced circuit failures involving unfused DC motor control  
14
circuits for Millstone Power Station Unit 3.  The postulated fire induced circuit failures could cause a secondary fire that could adversely affect fire safe shutdown equipment contrary to Unit 3 Renewed Facility Operating License Condition 2.H and the branch technical condition (BTP) 9.5-1 requirements.  The license  
The significance and enforcement aspect of this issue are discussed in Section 4OA7.2
of this inspection report.  LER 05000336/2014-002-00 (Unit 2) is closed.
.3  
(Closed) Licensee Event Report (LER) 05000423/2014-002-00 (Unit 3):  DC Circuit Hot  
Shorts  
   
On March 12, 2014, during a review of industry operating experience, Dominion  
identified postulated fire induced circuit failures involving unfused DC motor control  
circuits for Millstone Power Station Unit 3.  The postulated fire induced circuit  
failures could cause a secondary fire that could adversely affect fire safe shutdown  
equipment contrary to Unit 3 Renewed Facility Operating License Condition 2.H  
and the branch technical condition (BTP) 9.5-1 requirements.  The license  
condition and the BTP requires in part, post-fire safe shutdown cables remain free  
condition and the BTP requires in part, post-fire safe shutdown cables remain free  
of the effects of fire-induced cable faults during postulated fires.  Specifically, the  
of the effects of fire-induced cable faults during postulated fires.  Specifically, the  
licensee identified 125 V DC control circuits for non-safety related main turbine emergency lube oil and a main generator emergency seal oil pumps that were not provided with overcurrent protection.  Postulated fires in the turbine battery  
licensee identified 125 V DC control circuits for non-safety related main turbine  
emergency lube oil and a main generator emergency seal oil pumps that were not  
provided with overcurrent protection.  Postulated fires in the turbine battery  
switchgear area, the cable spreading room, the instrument rack room, and the  
switchgear area, the cable spreading room, the instrument rack room, and the  
control room could cause failure of the unprotected 125 V DC control circuits,  
control room could cause failure of the unprotected 125 V DC control circuits,  
which in turn could cause failure of control circuits for safe shutdown equipment.  Dominion determined the cause of the condition was a manufacturer's design error that involved the failure to include protective fuses in DC motor control  
which in turn could cause failure of control circuits for safe shutdown equipment.   
Dominion determined the cause of the condition was a manufacturers design  
error that involved the failure to include protective fuses in DC motor control  
circuits during plant construction.  
circuits during plant construction.  
  The licensee submitted LER 05000423/2014-002-00 (Unit 3) to report this event in accordance with 10 CFR 50.73(a)(2)(ii)(B) as an unanalyzed condition that significantly degraded plant safety.  The licensee entered this issue into their corrective action  
   
program as condition report number CR541983 and implemented compensatory measures in the affected fire areas pending final resolution of the issue.  
The licensee submitted LER 05000423/2014-002-00 (Unit 3) to report this event in  
  The licensee completed an engineering evaluation (RAS000253) of the issue and developed design change modifications (MP3-14-01071 and MP3-14-01092) to add overcurrent protection (fuses) to the affected motor control circuits.  Dominion completed the necessary modifications for all affected motor control circuits by November 2, 2014.
accordance with 10 CFR 50.73(a)(2)(ii)(B) as an unanalyzed condition that significantly  
  The significance and enforcement aspect of this issue are discussed in Section 4OA7.3 of this inspection report.  LER 05000289/2014-001-00 (Unit 3) is closed.  
degraded plant safety.  The licensee entered this issue into their corrective action  
   
program as condition report number CR541983 and implemented compensatory  
15  4OA6 Meetings, Including Exit
measures in the affected fire areas pending final resolution of the issue.  
  Exit Meeting Summary
   
  The team presented the inspection results to Mr. John Daugherty, Site Vice President, Millstone Power Station, and other members of the site staff at an exit meeting on August 11, 2016.  No proprietary information was included in this inspection report.
The licensee completed an engineering evaluation (RAS000253) of the issue and  
  4OA7 Licensee-Identified Violations
developed design change modifications (MP3-14-01071 and MP3-14-01092) to add  
  The following violations of very low safety significance (Green) were identified by the
overcurrent protection (fuses) to the affected motor control circuits.  Dominion completed  
the necessary modifications for all affected motor control circuits by November 2, 2014.  
The significance and enforcement aspect of this issue are discussed in Section 4OA7.3  
of this inspection report.  LER 05000289/2014-001-00 (Unit 3) is closed.  
   
   
   


licensee and are violations of NRC requirementsThese issues satisfy the criteria of the NRC Enforcement Policy of being dispositioned as Non-Cited Violations.
15
4OA6 Meetings, Including Exit
Exit Meeting Summary
The team presented the inspection results to Mr. John Daugherty, Site Vice President,
Millstone Power Station, and other members of the site staff at an exit meeting on
August 11, 2016.  No proprietary information was included in this inspection report.  
   
4OA7 Licensee-Identified Violations  
   
   
.1 LER 05000336/2013-003-00 (Unit 2) describes an unanalyzed condition in which Dominion identified their DC ammeter circuits were unfused.  Specifically, Dominion did not provide overcurrent protection for wiring associated with DC ammeter indication in  
The following violations of very low safety significance (Green) were identified by the
licensee and are violations of NRC requirements.  These issues satisfy the criteria of the
NRC Enforcement Policy of being dispositioned as Non-Cited Violations.
.1  
LER 05000336/2013-003-00 (Unit 2) describes an unanalyzed condition in which  
Dominion identified their DC ammeter circuits were unfused.  Specifically, Dominion did  
not provide overcurrent protection for wiring associated with DC ammeter indication in  
the control room to prevent wires from overheating due to fire induced faults and  
the control room to prevent wires from overheating due to fire induced faults and  
excessive currents flowing through the cable.  With enough current flowing through the  
excessive currents flowing through the cable.  With enough current flowing through the  
cable, the potential existed that the overloaded ammeter wiring could damage system wiring or adjacent safety-related circuits in the cable raceways needed for post-fire safe shutdown.  This condition could result in a loss of the associated safe shutdown  
cable, the potential existed that the overloaded ammeter wiring could damage system  
wiring or adjacent safety-related circuits in the cable raceways needed for post-fire safe  
shutdown.  This condition could result in a loss of the associated safe shutdown  
components or a secondary fire in another fire area.  The failure to protect safe  
components or a secondary fire in another fire area.  The failure to protect safe  
shutdown cables from the effects of postulated fires was a performance deficiency.  
shutdown cables from the effects of postulated fires was a performance deficiency.  
  This performance deficiency was a violation of Millstone Power Station, Unit 2, Renewed Facility Operating License Condition 2.C.(3), which requires in part, post-fire safe shutdown cables remain free of the effects of fire-induced cable faults during postulated  
   
This performance deficiency was a violation of Millstone Power Station, Unit 2, Renewed  
Facility Operating License Condition 2.C.(3), which requires in part, post-fire safe  
shutdown cables remain free of the effects of fire-induced cable faults during postulated  
fires.  Contrary to the above, Dominion identified they failed to meet this requirement and  
fires.  Contrary to the above, Dominion identified they failed to meet this requirement and  
the condition existed since initial construction of Unit 2.  The issue was more than minor  
the condition existed since initial construction of Unit 2.  The issue was more than minor  
because it was associated with the protection against external events (fire) attribute of the mitigating systems cornerstone and it adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating  
because it was associated with the protection against external events (fire) attribute of  
the mitigating systems cornerstone and it adversely affected the cornerstone objective of  
ensuring the availability, reliability, and capability of systems that respond to initiating  
events to prevent undesirable consequences.  The team determined that the finding was  
events to prevent undesirable consequences.  The team determined that the finding was  
of very low safety significance (Green), based IMC 0609, Appendix F, "Fire Protection  
of very low safety significance (Green), based IMC 0609, Appendix F, Fire Protection  
Significance Determination Process (SDP)," Phase 2 screening criteria.  
Significance Determination Process (SDP), Phase 2 screening criteria.  
  The finding screened to Green based upon, task number 2.3.5, because the  
   
The finding screened to Green based upon, task number 2.3.5, because the  
affected cables were routed in alternate shutdown fire areas that are continually  
affected cables were routed in alternate shutdown fire areas that are continually  
manned or protected by detection and  
manned or protected by detection and automatic suppression systems.   
automatic suppression systems.  Remaining fire areas are protected by detection systems, automatic suppression  
Remaining fire areas are protected by detection systems, automatic suppression  
systems or rely on manual fire-fighting activities.  Additionally, the cable construction is Institute of Electrical and Electronics Engineers (IEEE) 383 (thermoset) which decreases the likelihood of inter-cable and intra-cable  
systems or rely on manual fire-fighting activities.  Additionally, the cable  
construction is Institute of Electrical and Electronics Engineers (IEEE) 383  
(thermoset) which decreases the likelihood of inter-cable and intra-cable  
interactions.  Based on a team walkdown, the team determined that the ammeter  
interactions.  Based on a team walkdown, the team determined that the ammeter  
cable routing was not routed near a credible fire ignition source in the affected  
cable routing was not routed near a credible fire ignition source in the affected  
fire areas.  Because this finding is of very low safety significance and had been entered into Dominion's corrective action program (CR530987), this violation is   
fire areas.  Because this finding is of very low safety significance and had been  
16  being treated as a Green, licensee-identified NCV consistent with the NRC's Enforcement Policy.  
entered into Dominions corrective action program (CR530987), this violation is  
 
16
   
being treated as a Green, licensee-identified NCV consistent with the NRCs
Enforcement Policy.  
   
   
.2 LER 05000336/2014-002-00 (Unit 2) describes an unanalyzed condition in which Dominion identified DC motor control circuits were unfused.  Specifically, Dominion did not provide overcurrent protection for wiring associated with 125 V DC control circuits for a non-safety related main turbine emergency lube oil pump  
.2  
LER 05000336/2014-002-00 (Unit 2) describes an unanalyzed condition in which  
Dominion identified DC motor control circuits were unfused.  Specifically,  
Dominion did not provide overcurrent protection for wiring associated with 125 V  
DC control circuits for a non-safety related main turbine emergency lube oil pump  
to prevent wires from overheating due to fire induced faults and excessive  
to prevent wires from overheating due to fire induced faults and excessive  
currents flowing through the cable.  With enough current flowing through the  
currents flowing through the cable.  With enough current flowing through the  
cable, the potential existed that the overloaded motor control wiring could damage adjacent control circuit wiring for components which are needed to achieve and maintain post-fire safe shutdown for a fire in several fire areas (turbine battery  
cable, the potential existed that the overloaded motor control wiring could damage  
 
adjacent control circuit wiring for components which are needed to achieve and  
room, cable vault, plant equipment operator meeting area, control room).  This condition could result in a loss of the associated safe shutdown components or a  
maintain post-fire safe shutdown for a fire in several fire areas (turbine battery  
secondary fire in another fire area.  The failure to protect safe shutdown cables from the effect of postulated fires was a performance deficiency.  
room, cable vault, plant equipment operator meeting area, control room).  This  
  This performance deficiency was a violation of Millstone Power Station, Unit 2,  
condition could result in a loss of the associated safe shutdown components or a  
Renewed Facility Operating License Condition 2.C.(3), which requires, in part, post-fire safe shutdown cables remain free of the effects of fire induced cable faults during  
secondary fire in another fire area.  The failure to protect safe shutdown cables  
from the effect of postulated fires was a performance deficiency.  
   
This performance deficiency was a violation of Millstone Power Station, Unit 2,  
Renewed Facility Operating License Condition 2.C.(3), which requires, in part, post-fire  
safe shutdown cables remain free of the effects of fire induced cable faults during  
postulated fires.  Contrary to the above, Dominion identified they failed to meet this  
postulated fires.  Contrary to the above, Dominion identified they failed to meet this  
requirement and the condition existed since initial construction.  The issue was more than minor because it was associated with the protection against external events (fire) attribute of the mitigating systems cornerstone and it adversely affected the  
requirement and the condition existed since initial construction.  The issue was more  
cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.  The team  
than minor because it was associated with the protection against external events (fire)  
determined that the finding was of very low safety significance (Green), based on IMC 0609, Appendix F, "Fire Protection Significance Determination Process," Phase 2  
attribute of the mitigating systems cornerstone and it adversely affected the  
cornerstone objective of ensuring the availability, reliability, and capability of systems  
that respond to initiating events to prevent undesirable consequences.  The team  
determined that the finding was of very low safety significance (Green), based on IMC  
0609, Appendix F, Fire Protection Significance Determination Process, Phase 2  
screening criteria.  
screening criteria.  
  The finding screened to Green based upon, task number 2.3.5, because the affected cables were routed in alternate shutdown fire areas that are continually manned or  
   
The finding screened to Green based upon, task number 2.3.5, because the affected  
cables were routed in alternate shutdown fire areas that are continually manned or  
protected by detection and automatic suppression systems.  Remaining fire areas are  
protected by detection and automatic suppression systems.  Remaining fire areas are  
protected by detection systems, automatic suppression systems or rely on manual fire-fighting activities.  Additionally, the cable construction is IEEE 383 (thermoset) which decreases the likelihood of inter-cable and intra-cable interactions.  Based on a team walkdown, the team determined that the main turbine emergency lube oil pump cable routing was not routed near a credible fire ignition source in the affected fire areas.   
protected by detection systems, automatic suppression systems or rely on manual fire-
fighting activities.  Additionally, the cable construction is IEEE 383 (thermoset) which  
decreases the likelihood of inter-cable and intra-cable interactions.  Based on a team  
walkdown, the team determined that the main turbine emergency lube oil pump cable  
routing was not routed near a credible fire ignition source in the affected fire areas.   
Because this finding is of very low safety significance and had been entered into  
Because this finding is of very low safety significance and had been entered into  
Dominion's corrective action program (CR541980), this violation is being treated as a  
Dominions corrective action program (CR541980), this violation is being treated as a  
Green, licensee-identified NCV consistent with the NRC's Enforcement Policy.  
Green, licensee-identified NCV consistent with the NRCs Enforcement Policy.  
  .3 LER 05000423/2014-002-00 (Unit 3) describes an unanalyzed condition in which Dominion identified DC motor control circuits were unfused.  Specifically, Dominion did  
   
.3  
LER 05000423/2014-002-00 (Unit 3) describes an unanalyzed condition in which  
Dominion identified DC motor control circuits were unfused.  Specifically, Dominion did  
not provide overcurrent protection for wiring associated with 125 V DC control circuits for  
not provide overcurrent protection for wiring associated with 125 V DC control circuits for  
non-safety related main turbine emergency lube oil and main generator emergency seal oil pumps to prevent wires from overheating due to fire induced faults and excessive currents flowing through the cable.  With enough current flowing through the cable, the   
non-safety related main turbine emergency lube oil and main generator emergency seal  
17  potential existed that the overloaded motor control wiring could damage adjacent control circuit wiring for components which are needed to achieve and maintain post-fire safe  
oil pumps to prevent wires from overheating due to fire induced faults and excessive  
shutdown for a fire in several fire areas (turbine battery switchgear area, cable spreading room, instrument rack room, control room). This condition could result in a loss of the  
currents flowing through the cable.  With enough current flowing through the cable, the  
associated safe shutdown components or a secondary fire in another fire area.  The failure to protect safe shutdown cables from the effect of postulated fires was a performance deficiency.  
 
  This performance deficiency was a violation of Millstone Power Station, Unit 3,  
17
Renewed Facility Operating License Condition 2.H, which requires, in part, post-fire safe shutdown cables remain free of the effects of fire induced cable faults during postulated fires.  Contrary to the above, Dominion identified they failed to meet this requirement and the condition existed since initial construction.  The issue was more than minor because it was associated with the protection against external events (fire)  
   
potential existed that the overloaded motor control wiring could damage adjacent control  
circuit wiring for components which are needed to achieve and maintain post-fire safe  
shutdown for a fire in several fire areas (turbine battery switchgear area, cable spreading  
room, instrument rack room, control room). This condition could result in a loss of the  
associated safe shutdown components or a secondary fire in another fire area.  The  
failure to protect safe shutdown cables from the effect of postulated fires was a  
performance deficiency.  
   
This performance deficiency was a violation of Millstone Power Station, Unit 3,  
Renewed Facility Operating License Condition 2.H, which requires, in part, post-fire  
safe shutdown cables remain free of the effects of fire induced cable faults during  
postulated fires.  Contrary to the above, Dominion identified they failed to meet this  
requirement and the condition existed since initial construction.  The issue was more  
than minor because it was associated with the protection against external events (fire)  
attribute of the mitigating systems cornerstone and it adversely affected the  
attribute of the mitigating systems cornerstone and it adversely affected the  
cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.  The team determined that the finding was of very low safety significance (Green), based on IMC 0609, Appendix F, "Fire Protection Significance Determination Process," Phase 2  
cornerstone objective of ensuring the availability, reliability, and capability of systems  
that respond to initiating events to prevent undesirable consequences.  The team  
determined that the finding was of very low safety significance (Green), based on IMC  
0609, Appendix F, Fire Protection Significance Determination Process, Phase 2  
screening criteria.  
screening criteria.  
  The finding screened to Green based upon, task number 2.3.5, because the affected cables were routed in alternate shutdown fire areas that are continually manned or  
   
The finding screened to Green based upon, task number 2.3.5, because the affected  
cables were routed in alternate shutdown fire areas that are continually manned or  
protected by detection and automatic suppression systems.  Remaining fire areas are  
protected by detection and automatic suppression systems.  Remaining fire areas are  
protected by detection systems, automatic suppression systems or rely on manual fire-fighting activities.  Additionally, the cable construction is IEEE 383 (thermoset) which  
protected by detection systems, automatic suppression systems or rely on manual fire-
fighting activities.  Additionally, the cable construction is IEEE 383 (thermoset) which  
decreases the likelihood of inter-cable and intra-cable interactions.  Based on a team  
decreases the likelihood of inter-cable and intra-cable interactions.  Based on a team  
walkdown, the team determined that the main turbine emergency lube oil and main generator emergency seal oil pump cable routing was not routed near a credible fire ignition source in the affected fire areas.  Because this finding is of very low safety significance and had been entered into Dominion's corrective action program  
walkdown, the team determined that the main turbine emergency lube oil and main  
generator emergency seal oil pump cable routing was not routed near a credible fire  
ignition source in the affected fire areas.  Because this finding is of very low safety  
significance and had been entered into Dominions corrective action program  
(CR541983), this violation is being treated as a Green, licensee-identified NCV  
(CR541983), this violation is being treated as a Green, licensee-identified NCV  
consistent with the NRC's Enforcement Policy.  
consistent with the NRCs Enforcement Policy.  
 
ATTACHMENT:  SUPPLEMENTAL INFORMATION  
 
ATTACHMENT:  SUPPLEMENTAL INFORMATION
A-1  Attachment SUPPLEMENTAL INFORMATION
 
  KEY POINTS OF CONTACT  
A-1  
  Licensee Personnel J. Daugherty, Site Vice President D. Blakeney, Assistant Plant Manager P. Anastas, Safe Shutdown Engineer  
   
Attachment  
SUPPLEMENTAL INFORMATION  
KEY POINTS OF CONTACT  
   
Licensee Personnel  
J. Daugherty, Site Vice President  
D. Blakeney, Assistant Plant Manager  
P. Anastas, Safe Shutdown Engineer  
J. Armstrong, Fire Protection Engineer  
J. Armstrong, Fire Protection Engineer  
T. Bryant, Maintenance Supervisor  
T. Bryant, Maintenance Supervisor  
D. DelBiondo, Site Fire Marshal J. Farley, Electrical System Engineer  
D. DelBiondo, Site Fire Marshal  
J. Farley, Electrical System Engineer  
B. Ferguson, Unit 2 Senior Reactor Operator  
B. Ferguson, Unit 2 Senior Reactor Operator  
R. Garver, Engineering Director  
R. Garver, Engineering Director  
L. Kelly, Engineering Lead  
L. Kelly, Engineering Lead  
W. McCollum, Unit 2 Supervisor  
W. McCollum, Unit 2 Supervisor  
D. Mello, Senior Fire Instructor K. Perkins, Electrical Engineering Supervisor P. Russell, Unit 3 Senior Reactor Operator  
D. Mello, Senior Fire Instructor  
K. Perkins, Electrical Engineering Supervisor  
P. Russell, Unit 3 Senior Reactor Operator  
A. Vargas-Mendez, Licensing Engineer  
A. Vargas-Mendez, Licensing Engineer  
   
   
NRC Personnel C. Cahill, Acting Branch Chief, Engineering Brach 3, Division of Reactor Safety  
NRC Personnel  
C. Cahill, Acting Branch Chief, Engineering Brach 3, Division of Reactor Safety  
C. Highley, Resident Inspector, Millstone Power Station  
C. Highley, Resident Inspector, Millstone Power Station  
L. Mckown, Resident Inspector, Millstone Power Station   
L. Mckown, Resident Inspector, Millstone Power Station   
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened None 
   
   
Opened and Closed 05000336/2016007-01 NCV Unapproved OMA in Lieu of Meeting III.G.2 Fire  
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Protection Requirements for Fire Area R-14, Lower 4kV Switchgear Room and Cable Vault  
Opened
None 
Opened and Closed  
05000336/2016007-01  
NCV  
Unapproved OMA in Lieu of Meeting III.G.2 Fire  
Protection Requirements for Fire Area R-14, Lower  
4kV Switchgear Room and Cable Vault  
Closed
05000336/2013-003-00
LER
Postulated DC Ammeter Circuit Hot Shorts (Unit 2),
(Section 4OA3.1)
05000336/2014-002-00
LER
DC Circuit Hot Shorts (Unit 2), (Section 4OA3.2)
   
   
Closed 05000336/2013-003-00 LER Postulated DC Ammeter Circuit Hot Shorts (Unit 2), (Section 4OA3.1)  
05000423/2014-002-00  
LER  
DC Circuit Hot Shorts (Unit 3), (Section 4OA3.3)  
   
   
05000336/2014-002-00 LER DC Circuit Hot Shorts (Unit 2), (Section 4OA3.2)
Discussed
None


A-2
LIST OF DOCUMENTS REVIEWED
   
   
05000423/2014-002-00 LER DC Circuit Hot Shorts (Unit 3), (Section 4OA3.3)
Fire Protection Licensing Documents  
 
25203-SP-M2-SU-1046, Unit 2 Appendix R Compliance Report, Revision 1  
Discussed
None 
A-2  LIST OF DOCUMENTS REVIEWED
Fire Protection Licensing Documents 25203-SP-M2-SU-1046, Unit 2 Appendix R Compliance Report, Revision 1  
 
25212-BTP-9.5-1, Unit 3 Branch Technical Position 9.5-1 Compliance Report, Revision 4  
25212-BTP-9.5-1, Unit 3 Branch Technical Position 9.5-1 Compliance Report, Revision 4  
25212-MP3-SFR, Millstone Power Station, Unit 3, Safety Function Requirement Manual, Revision 6 LBDCR 07-MP2-010, Millstone U2 Technical Requirements, dated 10/5/09  
25212-MP3-SFR, Millstone Power Station, Unit 3, Safety Function Requirement Manual,  
Letter from Dominion to NRC, Dominion Nuclear Connecticut, Inc. Millstone Power Station Unit 2 Response to Request for Additional Information Request for Exemption from   
Revision 6  
10 CFR 50, Appendix R, Section III.G., Fire Protection of Safe Shutdown Capability, with Attachment, dated 2/29/12 Letter from Dominion to NRC, Dominion Nuclear Connecticut, Inc. Millstone Power Station Unit 2 Request for a Revision of an Exemption from 10 CFR 50, Appendix R, Section III.G.,  
LBDCR 07-MP2-010, Millstone U2 Technical Requirements, dated 10/5/09  
Fire Protection of Safe Shutdown Capability, with Attachment, dated 10/29/12 Letter from Dominion to NRC, Dominion Nuclear Connecticut. Inc. Millstone Power Station Unit 2 Request for Exemption from 10 CFR 50. Appendix R. Section III.G., Fire Protection of  
Letter from Dominion to NRC, Dominion Nuclear Connecticut, Inc. Millstone Power Station Unit  
Safe Shutdown Capability, with Attachments, dated 6/30/11 Letter from NRC to Dominion, Millstone Power Station, Unit 2 -Correction to Previously Issued Exemption from the Requirements of 10 CFR Part 50, Appendix R, Section III.G.2.   
2 Response to Request for Additional Information Request for Exemption from   
(TAC No. ME6693) with Enclosure, dated 12/18/12 Millstone Unit 2 Technical Requirement Manual, Section 3/4.7.9, Fire Protection System, 2/2/10 Millstone Unit 3 Fire Protection Evaluation Report, Revision 17.4 MP-SPEC-ENG-BTP-9.5-1, Millstone Unit 3 Branch Technical Position (BTP) 9.5-1 Compliance Report, Revision 4 U2-24-FPP-FHA, Unit 2 Fire Hazards Analysis, Revision 12  
10 CFR 50, Appendix R, Section III.G., Fire Protection of Safe Shutdown Capability, with  
Attachment, dated 2/29/12  
Letter from Dominion to NRC, Dominion Nuclear Connecticut, Inc. Millstone Power Station Unit  
2 Request for a Revision of an Exemption from 10 CFR 50, Appendix R, Section III.G.,  
Fire Protection of Safe Shutdown Capability, with Attachment, dated 10/29/12  
Letter from Dominion to NRC, Dominion Nuclear Connecticut. Inc. Millstone Power Station Unit  
2 Request for Exemption from 10 CFR 50. Appendix R. Section III.G., Fire Protection of  
Safe Shutdown Capability, with Attachments, dated 6/30/11  
Letter from NRC to Dominion, Millstone Power Station, Unit 2 -Correction to Previously Issued  
Exemption from the Requirements of 10 CFR Part 50, Appendix R, Section III.G.2.   
(TAC No. ME6693) with Enclosure, dated 12/18/12  
Millstone Unit 2 Technical Requirement Manual, Section 3/4.7.9, Fire Protection System, 2/2/10  
Millstone Unit 3 Fire Protection Evaluation Report, Revision 17.4  
MP-SPEC-ENG-BTP-9.5-1, Millstone Unit 3 Branch Technical Position (BTP) 9.5-1 Compliance  
Report, Revision 4  
U2-24-FPP-FHA, Unit 2 Fire Hazards Analysis, Revision 12  
Updated Final Safety Analysis Report, Section 9.5.1, Fire Protection System, Revision 28.2  
Updated Final Safety Analysis Report, Section 9.5.1, Fire Protection System, Revision 28.2  
Design Basis Documents Fire Code Compliance Review of Safety Related Areas - Fire Protection Systems -Fire Alarm/Detection Systems and the plants Fire Pumps, dated 9/86 TR-151, Fire and Hose Stream Test of #TCO-003 High Density Silicone Elastomer used in Elec.
Opening, Revision 0 TR-189, Fire and Hose Stream Test of 6", 8", and 10" thick specimens of TCO-050, Revision 1
   
   
Design Changes DCN DM3-00-1286-97, Revision to the BTP 9.5-1 Compliance Report to Include RHS MOVs, dated 2/5/98 DCR M2-97034, Thermo-Lag Modifications for MP2, Revision 0  
Design Basis Documents
Fire Code Compliance Review of Safety Related Areas - Fire Protection Systems -Fire
Alarm/Detection Systems and the plants Fire Pumps, dated 9/86
TR-151, Fire and Hose Stream Test of #TCO-003 High Density Silicone Elastomer used in Elec.
Opening, Revision 0
TR-189, Fire and Hose Stream Test of 6, 8, and 10 thick specimens of TCO-050, Revision 1
Design Changes  
DCN DM3-00-1286-97, Revision to the BTP 9.5-1 Compliance Report to Include RHS MOVs,  
dated 2/5/98  
DCR M2-97034, Thermo-Lag Modifications for MP2, Revision 0  
M2-98095, TDAFWP Redundant Power Supply, Revision 0  
M2-98095, TDAFWP Redundant Power Supply, Revision 0  
MP2-14-01007, DC Ammeter Hot Short Modification, Revision 1  
MP2-14-01007, DC Ammeter Hot Short Modification, Revision 1  
MP2-14-01040, Appendix R Hot Short Circuit Modification for Emergency Bearing Oil Pump  
MP2-14-01040, Appendix R Hot Short Circuit Modification for Emergency Bearing Oil Pump  
P63, Revision 1 MP3-13-01183, RHR Cross-Train Suction Motor-Operated Valve Breaker Normal Alignment Change, dated 10/29/13 MP3-14-01071, Appendix R Hot Short Circuit Modification for Emergency Bearing Oil Pump  
P63, Revision 1  
MP3-13-01183, RHR Cross-Train Suction Motor-Operated Valve Breaker Normal Alignment  
Change, dated 10/29/13  
MP3-14-01071, Appendix R Hot Short Circuit Modification for Emergency Bearing Oil Pump  
3TML-P1, Revision 0  
3TML-P1, Revision 0  
 
A-3   MP3-14-01092, Appendix R Hot Short Circuit Modification for Emergency Seal Oil Pump 3GMO-P2, Revision 0 MP3-14-01187, MP3 RPCCW Heat Exchanger 3CCP*E1B Replacement, dated 7/6/15  
 
A-3  
MP3-14-01092, Appendix R Hot Short Circuit Modification for Emergency Seal Oil Pump  
3GMO-P2, Revision 0  
MP3-14-01187, MP3 RPCCW Heat Exchanger 3CCP*E1B Replacement, dated 7/6/15  
MPG-13-01131, MDM Flex Strategy Support Modification, dated 9/16/14  
MPG-13-01131, MDM Flex Strategy Support Modification, dated 9/16/14  
   
   
Calculations/Engineering Evaluation Reports 25203-ER-98-0151, Fire Test Performed for Florida Power & Light Company for Electrical Raceways Protected with Thermo-Lag Fire Barrier Systems, Revision, 0 25203-ER-99-0092, Millstone Unit 2 Appendix R Cooldown Analysis Assumptions and Results, Revision 3 97-ENG-01912E2, 4.16kV Switchgear Relay Settings, Revision 0 98-ENG-02411-C2, MP2 Evaluation Flooding Outside Containment, Revision 1 98-ENG-02621-M2, Determination of the Instrument Air Requirement for Certain Safety Related Valves, Revision 3 99-026, Calculation Change Notice No. 1, Millstone Site Fire Loop Flow Model Bench Markings, Revision 1 99-026, Calculation Change Notice No. 3, Millstone Site Fire Loop Flow Model Bench Markings, Revision 1 99-026, Calculation Change Notice No. 4, Millstone Site Fire Loop Flow Model Bench Markings, Revision 1 99-026, Millstone Site Fire Loop Flow Model Bench Markings, Revision 1  
Calculations/Engineering Evaluation Reports  
DNC 2512-ER-04-0030, Validation and Verification of EOP 3509.1 Using Simulator, Field and Table Top Validation, dated 5/28/04 EMP-186, Millstone Nuclear Power Plant U2 Combustible Loading Re-Analysis Calculation, Revision 2 ER-97-0295, Sound Powered Phone and Trunked Radio Systems - Cable Selection, Routing and Figures, dated 1/16/98 ER-97-0302, MP3 BTP 9.5-1 Compliance Report Section 6.2 Revision - Communication Systems, dated 2/10/98 M2-EV-98-0113, Technical Evaluation for 120Vac Vital Bus Appendix R Coordination Study, Revision 1 M3-EV-98-0011, Technical Evaluation for The Use of an 800 MHz Carrier Frequency Trunked Radio System at Millstone Unit 3 for General Purposes and Appendix R Requirements, Revision 1 MP-CALC-ENG-S-0426535, MP3 BTP 9.5-1 RELAP5 Fire Shutdown Analysis 3650 and 3725 MWt, Revision 2 P1164-MP2-COORD, Unit 2 Breaker/Fuse Coordination for the Appendix R Circuits, Revision 0  
25203-ER-98-0151, Fire Test Performed for Florida Power & Light Company for Electrical  
RAS000244, Postulated DC Ammeter Circuit Hot Shorts, Revision 0 RAS000252, DC Circuit Hot Shorts, Revision 0 RAS000253, DC Circuit Hot Shorts, Revision 0  
Raceways Protected with Thermo-Lag Fire Barrier Systems, Revision, 0  
25203-ER-99-0092, Millstone Unit 2 Appendix R Cooldown Analysis Assumptions and Results,  
Revision 3  
97-ENG-01912E2, 4.16kV Switchgear Relay Settings, Revision 0  
98-ENG-02411-C2, MP2 Evaluation Flooding Outside Containment, Revision 1  
98-ENG-02621-M2, Determination of the Instrument Air Requirement for Certain Safety Related  
Valves, Revision 3  
99-026, Calculation Change Notice No. 1, Millstone Site Fire Loop Flow Model Bench Markings,  
Revision 1  
99-026, Calculation Change Notice No. 3, Millstone Site Fire Loop Flow Model Bench Markings,  
Revision 1  
99-026, Calculation Change Notice No. 4, Millstone Site Fire Loop Flow Model Bench Markings,  
Revision 1  
99-026, Millstone Site Fire Loop Flow Model Bench Markings, Revision 1  
DNC 2512-ER-04-0030, Validation and Verification of EOP 3509.1 Using Simulator, Field and  
Table Top Validation, dated 5/28/04  
EMP-186, Millstone Nuclear Power Plant U2 Combustible Loading Re-Analysis Calculation,  
Revision 2  
ER-97-0295, Sound Powered Phone and Trunked Radio Systems - Cable Selection, Routing  
and Figures, dated 1/16/98  
ER-97-0302, MP3 BTP 9.5-1 Compliance Report Section 6.2 Revision - Communication  
Systems, dated 2/10/98  
M2-EV-98-0113, Technical Evaluation for 120Vac Vital Bus Appendix R Coordination Study,  
Revision 1  
M3-EV-98-0011, Technical Evaluation for The Use of an 800 MHz Carrier Frequency Trunked  
Radio System at Millstone Unit 3 for General Purposes and Appendix R Requirements,  
Revision 1  
MP-CALC-ENG-S-0426535, MP3 BTP 9.5-1 RELAP5 Fire Shutdown Analysis 3650 and 3725  
MWt, Revision 2  
P1164-MP2-COORD, Unit 2 Breaker/Fuse Coordination for the Appendix R Circuits, Revision 0  
RAS000244, Postulated DC Ammeter Circuit Hot Shorts, Revision 0  
RAS000252, DC Circuit Hot Shorts, Revision 0  
RAS000253, DC Circuit Hot Shorts, Revision 0  
S-02824S2, Millstone Unit 2, R-2 Fire, Appendix R Analysis, Revision 2  
S-02824S2, Millstone Unit 2, R-2 Fire, Appendix R Analysis, Revision 2  
SP-M3-EE-269, Unit 3 Electrical Design Criteria, Revision 3  
SP-M3-EE-269, Unit 3 Electrical Design Criteria, Revision 3  
W2-517-744-RE, MP2 Appendix R Cooldown, Revision 3  
W2-517-744-RE, MP2 Appendix R Cooldown, Revision 3  


   
A-4  
A-4   Procedures 3783EA, Component Cooling Pump Motor Replacement for Fire Protection, Revision 005-02 C MP 790, Emergency Light Inspection and Testing, Revision 004-02  
Procedures  
3783EA, Component Cooling Pump Motor Replacement for Fire Protection, Revision 005-02  
C MP 790, Emergency Light Inspection and Testing, Revision 004-02  
C OP 200.18, Time Critical Action Validation and Verification, Revision 2  
C OP 200.18, Time Critical Action Validation and Verification, Revision 2  
C OP 200.18, Time Critical Action Validation and Verification, Revision 3  
C OP 200.18, Time Critical Action Validation and Verification, Revision 3  
C SP 600.24, Fire Brigade Equipment Inspection, Revision 000-04 C SP 600.28, Fire Brigade vehicle Equipment Inspection Data Sheet (R3), Revision 000-05 C SP600.24, Unit 2 Fire Brigade Equipment Inspection, Revision 001-00  
C SP 600.24, Fire Brigade Equipment Inspection, Revision 000-04  
C SP 600.28, Fire Brigade vehicle Equipment Inspection Data Sheet (R3), Revision 000-05  
C SP600.24, Unit 2 Fire Brigade Equipment Inspection, Revision 001-00  
CM-AA-ETE-101, Engineering Technical Evaluation (ETE), Revision 6  
CM-AA-ETE-101, Engineering Technical Evaluation (ETE), Revision 6  
CM-AA-FPA-10, Fire Protection/Appendix R (Fire Safe Shutdown) Program, Revision 2  
CM-AA-FPA-10, Fire Protection/Appendix R (Fire Safe Shutdown) Program, Revision 2  
CM-AA-FPA-100, Fire Protection/Appendix R (Fire Safe Shutdown) Program, Revision 11 CM-AA-FPA-101, Control of Combustible and Flammable Materials, Revision 8 CM-AA-FPA-102, Fire Protection and Fire Safe Shutdown review and preparation Process and Preparation Process and Design Change Process, Revision 6 COM-04-C, Plant Communication Systems, Revision 0  
CM-AA-FPA-100, Fire Protection/Appendix R (Fire Safe Shutdown) Program, Revision 11  
CM-AA-FPA-101, Control of Combustible and Flammable Materials, Revision 8  
CM-AA-FPA-102, Fire Protection and Fire Safe Shutdown review and preparation Process and  
Preparation Process and Design Change Process, Revision 6  
COM-04-C, Plant Communication Systems, Revision 0  
ER-AA-102, Preventive Maintenance Program, Revision 9  
ER-AA-102, Preventive Maintenance Program, Revision 9  
ER-AA-MRL-100, Implementing Maintenance Rule, Revision 10 FB-00012, Self-Contained Breathing Apparatus SCOTT 4.5, Revision 7 MP 2720U1, Cold Shutdown Fire Damage Repair Procedure for Fire Area R-1 (Appendix R), Revision 004-02 SA-AA-115, Conduct of Fire Drills, Revision 2  
ER-AA-MRL-100, Implementing Maintenance Rule, Revision 10  
SFP 10, Fire Protection Inspections, Revision 005-03 SFP 21, Appendix R Fire Cage Inventory, Revision 002-06 SP 2402CR, Steam Generator Pressure Rack Instrument Calibration, Revision 0  
FB-00012, Self-Contained Breathing Apparatus SCOTT 4.5, Revision 7  
MP 2720U1, Cold Shutdown Fire Damage Repair Procedure for Fire Area R-1 (Appendix R),  
Revision 004-02  
SA-AA-115, Conduct of Fire Drills, Revision 2  
SFP 10, Fire Protection Inspections, Revision 005-03  
SFP 21, Appendix R Fire Cage Inventory, Revision 002-06  
SP 2402CR, Steam Generator Pressure Rack Instrument Calibration, Revision 0  
SP 2601P, CVCS Valve Operability Tests From C-10 and C-02, Revision 0  
SP 2601P, CVCS Valve Operability Tests From C-10 and C-02, Revision 0  
SP 2610B, Turbine Driven Auxiliary Feed Pump O
SP 2610B, Turbine Driven Auxiliary Feed Pump Operational Tests from C-10, Revision 1  
perational Tests from C-10, Revision 1 SP 2610E, Atmospheric Dump Valve Testing from C-10, C-70A and C-70B, Revision 1 SP 2610M, Power Operated Relief Valve Hot Functional Test, Revision 0 SP 3442J01, RCS Wide Range Pressure Rack Calibration, Revision 7  
SP 2610E, Atmospheric Dump Valve Testing from C-10, C-70A and C-70B, Revision 1  
SP 2610M, Power Operated Relief Valve Hot Functional Test, Revision 0  
SP 3442J01, RCS Wide Range Pressure Rack Calibration, Revision 7  
SP 3444A02, Steam Generator Water Level Wide Range Calibration, Revision 7  
SP 3444A02, Steam Generator Water Level Wide Range Calibration, Revision 7  
SP 3641D.3, Fire Detection and Control System Operability Check, Revision 015  
SP 3641D.3, Fire Detection and Control System Operability Check, Revision 015  
SP 3641D.5, Fire Damper Operability Verification, Revision 012  
SP 3641D.5, Fire Damper Operability Verification, Revision 012  
SP 3641F.1, Functional Check of the East and West Switchgear Breathing Air Systems, Revision 2 SP 3673.2, Fire Transfer Switch Panel Operational Testing, Revision 002-06  
SP 3641F.1, Functional Check of the East and West Switchgear Breathing Air Systems,  
Revision 2  
SP 3673.2, Fire Transfer Switch Panel Operational Testing, Revision 002-06  
SP 3673.4, Auxiliary Shutdown Panel Operability Test, Revision 010  
SP 3673.4, Auxiliary Shutdown Panel Operability Test, Revision 010  
TR-MP-TPG-2300, Fire Protection Programs Training Program Guide (TPG), Revision 2  
TR-MP-TPG-2300, Fire Protection Programs Training Program Guide (TPG), Revision 2  
WC5, Fuse Control, Revision 2  
WC5, Fuse Control, Revision 2  
  Operations Procedures AOP 2559, Millstone Unit 2 Fire, Revision 10  
   
Operations Procedures  
AOP 2559, Millstone Unit 2 Fire, Revision 10  
AOP 2559, Procedure Basis Document, Fire, Revision 009-00  
AOP 2559, Procedure Basis Document, Fire, Revision 009-00  
AOP 2579A, Fire Procedure for Hot Standby Appendix R Fire Area R-1, Revision 011-00  
AOP 2579A, Fire Procedure for Hot Standby Appendix R Fire Area R-1, Revision 011-00  
AOP 2579A, Procedure Basis Document, Fire Procedure for Hot Standby Appendix R Fire Area  
AOP 2579A, Procedure Basis Document, Fire Procedure for Hot Standby Appendix R Fire Area  
R-1, Revision 011-00 AOP 2579A, Unit 2 Fire Procedure for Hot Standby Appendix R Fire Area R-1, Revision 11  
R-1, Revision 011-00  
AOP 2579AA, Fire Procedure for Cooldown and Cold Shutdown, Appendix R Fire Area R-1, Revision 004-08
AOP 2579A, Unit 2 Fire Procedure for Hot Standby Appendix R Fire Area R-1, Revision 11  
A-5   AOP 2579EE, Fire Procedure for Cooldown and Cold Shutdown, Appendix R Fire Area R-7, R-9, R-14, and R-17, Revision 005-09 AOP 2579G, Fire Procedure for Hot Standby Appendix R Fire Area R-7, Revision 006-10  
AOP 2579AA, Fire Procedure for Cooldown and Cold Shutdown, Appendix R Fire Area R-1,  
Revision 004-08  
 
A-5  
AOP 2579EE, Fire Procedure for Cooldown and Cold Shutdown, Appendix R Fire Area R-7, R-
9, R-14, and R-17, Revision 005-09  
AOP 2579G, Fire Procedure for Hot Standby Appendix R Fire Area R-7, Revision 006-10  
AOP 2579M, Fire Procedure for Hot Standby Appendix R Fire Area R-14, Revision 006-06  
AOP 2579M, Fire Procedure for Hot Standby Appendix R Fire Area R-14, Revision 006-06  
AOP 3577, Loss of Normal and Offsite Power to a 4.16 kV Emergency Bus, Revision 003  
AOP 3577, Loss of Normal and Offsite Power to a 4.16 kV Emergency Bus, Revision 003  
AOP 3577, Procedure Basis Document, Loss of Normal and Offsite Power to a 4.16 kV Emergency Bus, Revision 002-00 AOP 3581, Immediate Operator Actions, Revision 003  
AOP 3577, Procedure Basis Document, Loss of Normal and Offsite Power to a 4.16 kV  
COP 200.2AIR, "Airborne Threat," Revision 002-03  
Emergency Bus, Revision 002-00  
AOP 3581, Immediate Operator Actions, Revision 003  
COP 200.2AIR, Airborne Threat, Revision 002-03  
EDMG 2.01, MP2 B.5.b Event Control Room Response, Revision 004  
EDMG 2.01, MP2 B.5.b Event Control Room Response, Revision 004  
EDMG 2.02, MP2 B.5.b Event TSC Response, Revision 010 EOP 2540, Functional Recovery, Revision 025-00 EOP 2540D, Functional Recovery of Heat Removal, Revision 022-00  
EDMG 2.02, MP2 B.5.b Event TSC Response, Revision 010  
EOP 2540, Functional Recovery, Revision 025-00  
EOP 2540D, Functional Recovery of Heat Removal, Revision 022-00  
EOP 2541, Appendix 36, ADV Local Operation, Revision 000-02  
EOP 2541, Appendix 36, ADV Local Operation, Revision 000-02  
EOP 2541, Appendix 7, TDAFW Pump Abnormal Startup, Revision 000-01  
EOP 2541, Appendix 7, TDAFW Pump Abnormal Startup, Revision 000-01  
EOP 2541, Standard Appendices, Revision 006  
EOP 2541, Standard Appendices, Revision 006  
EOP 35 GA-31, Locally Restoring AFW Flow, Revision 004 EOP 3509, Fire Emergency, Revision 027-00 EOP 3509, Procedure Basis Document, Fire Emergency, Revision 026-00  
EOP 35 GA-31, Locally Restoring AFW Flow, Revision 004  
EOP 3509, Fire Emergency, Revision 027-00  
EOP 3509, Procedure Basis Document, Fire Emergency, Revision 026-00  
EOP 3509.1, Control Room, Cable Spreading Area or Instrument Rack Room Fire,   
EOP 3509.1, Control Room, Cable Spreading Area or Instrument Rack Room Fire,   
Revision 019-00 EOP 3509.1, Procedure Basis Document, Control Room, Cable Spreading Area or Instrument Rack Room Fire, Revision 019-00 EOP 3509.15, North (A) EDG Enclosure or East (A) F.O. Vault Fire, Revision 001   
Revision 019-00  
EOP 3509.1, Procedure Basis Document, Control Room, Cable Spreading Area or Instrument  
Rack Room Fire, Revision 019-00  
EOP 3509.15, North (A) EDG Enclosure or East (A) F.O. Vault Fire, Revision 001   
EOP 3509.15, Procedure Basis Document, North (A) EDG Enclosure or East (A) F.O. Vault  
EOP 3509.15, Procedure Basis Document, North (A) EDG Enclosure or East (A) F.O. Vault  
Fire, Revision 001 EOP 3509.19, ESF Building North RHR Heat Exchanger Cubicle Fire, Revision 000-01 EOP 3509.19, Procedure Basis Document, ESF Building North RHR Heat Exchanger Cubicle  
Fire, Revision 001  
Fire, Revision 000-01 EOP 3509.6, Auxiliary Building West MCC/Rod Control/ACU Area Fire, Revision 002-01  
EOP 3509.19, ESF Building North RHR Heat Exchanger Cubicle Fire, Revision 000-01  
EOP 3509.19, Procedure Basis Document, ESF Building North RHR Heat Exchanger Cubicle  
Fire, Revision 000-01  
EOP 3509.6, Auxiliary Building West MCC/Rod Control/ACU Area Fire, Revision 002-01  
EOP 3509.6, Procedure Basis Document, Auxiliary Building West MCC/Rod Control/ACU Area  
EOP 3509.6, Procedure Basis Document, Auxiliary Building West MCC/Rod Control/ACU Area  
Fire, Revision 002-01 MP-PROC-OPS-OP-2322, Auxiliary Feedwater System, Revision 029 OP 2343, 4160 Volt Electrical System, Revision 022 OP 3341B, Fire Protection Halon System, Revision 005-06  
Fire, Revision 002-01  
MP-PROC-OPS-OP-2322, Auxiliary Feedwater System, Revision 029  
OP 2343, 4160 Volt Electrical System, Revision 022  
OP 3341B, Fire Protection Halon System, Revision 005-06  
OP 3353.MB4A, Main Board 4A Annunciator Response, Revision 003  
OP 3353.MB4A, Main Board 4A Annunciator Response, Revision 003  
OP 3353.MB4B, Main Board 4B Annunciator Response, Revision 005  
OP 3353.MB4B, Main Board 4B Annunciator Response, Revision 005  
OP-3322, Auxiliary Feedwater System, Revision 025 SACRG-3, Severe Accident CR Guideline for MP3 B.5.b Initial Event Response, Revision 004 SAG-1, Injection into the Steam Generators, Revision 011  
OP-3322, Auxiliary Feedwater System, Revision 025  
SACRG-3, Severe Accident CR Guideline for MP3 B.5.b Initial Event Response, Revision 004  
SAG-1, Injection into the Steam Generators, Revision 011  
SAG-2, Depressurize the RCS, Revision 003  
SAG-2, Depressurize the RCS, Revision 003  
SAG-9, MP3 B.5.b Event TSC Response (EDMG), Revision 016  
SAG-9, MP3 B.5.b Event TSC Response (EDMG), Revision 016  
SP 2669A, Unit 2 Auxiliary Building Rounds, Revision 063  
SP 2669A, Unit 2 Auxiliary Building Rounds, Revision 063  


   
A-6  
A-6   Completed Tests/Surveillances 722481, B.5.b pump annual preventive maintenance, Completed 7/26/16 C OP 200.18, Time Critical Action Validation and Verification, Completed 8/4/16  
Completed Tests/Surveillances  
722481, B.5.b pump annual preventive maintenance, Completed 7/26/16  
C OP 200.18, Time Critical Action Validation and Verification, Completed 8/4/16  
C SP 600.13, P-82 Electric Fire Pump Annual Operability Demonstration, Completed 5/19/16 &  
C SP 600.13, P-82 Electric Fire Pump Annual Operability Demonstration, Completed 5/19/16 &  
9/17/16 C SP 600.14, P-82 Electric Fire Pump Annual Operability Demonstration, Completed 12/4/14 &  
9/17/16  
12/4/15 C SP 600.16 Fire Protection System Underground Main Flush & Flow Test, Completed 10/13/10  
C SP 600.14, P-82 Electric Fire Pump Annual Operability Demonstration, Completed 12/4/14 &  
& 10/9/13 C SP 600.18, Unit 2 Fire Hose Station Inspection, Completed 6/22/16  
12/4/15  
C SP 600.22, Unit 2 Fire Hose Station Flow Test, Completed 2/13/15 C SP 600.24, Unit 2 Fire Brigade Equipment Inspection, Completed 4/24/16 C SP 600.24, Unit 2 Fire Brigade Equipment Inspection, Completed 5/25/16  
C SP 600.16 Fire Protection System Underground Main Flush & Flow Test, Completed 10/13/10  
& 10/9/13  
C SP 600.18, Unit 2 Fire Hose Station Inspection, Completed 6/22/16  
C SP 600.22, Unit 2 Fire Hose Station Flow Test, Completed 2/13/15  
C SP 600.24, Unit 2 Fire Brigade Equipment Inspection, Completed 4/24/16  
C SP 600.24, Unit 2 Fire Brigade Equipment Inspection, Completed 5/25/16  
C SP 600.25, Unit 2 Fire Door Inspection, Completed 6/20/16  
C SP 600.25, Unit 2 Fire Door Inspection, Completed 6/20/16  
C SP 600.25, Unit 3 Fire Door Inspection, Completed 9/3/15  
C SP 600.25, Unit 3 Fire Door Inspection, Completed 9/3/15  
C SP 600.28, Fire Brigade Vehicle Equipment Inspection Data Sheet (R1), Completed 5/21/16  
C SP 600.28, Fire Brigade Vehicle Equipment Inspection Data Sheet (R1), Completed 5/21/16  
C SP 600.6, Electric Fire Pump M7-8 Monthly Operability Demonstration, Completed 5/10/16 &  
C SP 600.6, Electric Fire Pump M7-8 Monthly Operability Demonstration, Completed 5/10/16 &  
6/3/16 C SP 600.7, Electric Fire Pump M7-8 Annual Operability Demonstration, Completed 12/22/14 &  
6/3/16  
12/19/15 C SP 600.8, Diesel Fire Pump M7-7 Monthly Operability Demonstration, Completed 5/13/16 &  
C SP 600.7, Electric Fire Pump M7-8 Annual Operability Demonstration, Completed 12/22/14 &  
6/8/16 C SP 600.9, Diesel Fire Pump M7-7 Annual Operability Demonstration, Completed 8/6/15 &  
12/19/15  
6/8/16 C SP 788A, Fire Pump Diesel Engine Battery Quarterly Surveillance, Completed 6/16/16  
C SP 600.8, Diesel Fire Pump M7-7 Monthly Operability Demonstration, Completed 5/13/16 &  
6/8/16  
C SP 600.9, Diesel Fire Pump M7-7 Annual Operability Demonstration, Completed 8/6/15 &  
6/8/16  
C SP 788A, Fire Pump Diesel Engine Battery Quarterly Surveillance, Completed 6/16/16  
C SP 788B, Fire Pump Diesel Engine Battery 18-Month Surveillance, Completed 6/10/16  
C SP 788B, Fire Pump Diesel Engine Battery 18-Month Surveillance, Completed 6/10/16  
C SP 788C, Fire Pump Diesel Engine Battery Weekly Surveillance, Completed 6/16/16 CSP 600.24, Fire Brigade Equipment Inspection, Completed 6/3/16 SFP 17, Unit 3 Fire Penetration Seal and Barrier Inspection- Group 1, Completed 2/10/06  
C SP 788C, Fire Pump Diesel Engine Battery Weekly Surveillance, Completed 6/16/16  
CSP 600.24, Fire Brigade Equipment Inspection, Completed 6/3/16  
SFP 17, Unit 3 Fire Penetration Seal and Barrier Inspection- Group 1, Completed 2/10/06  
SFP 17, Unit 3 Fire Penetration Seal and Barrier Inspection- Group 4, Completed 2/9/11  
SFP 17, Unit 3 Fire Penetration Seal and Barrier Inspection- Group 4, Completed 2/9/11  
SFP 17, Unit 3 Fire Penetration Seal and Barrier Inspection- Group 4, Completed 10/9/14  
SFP 17, Unit 3 Fire Penetration Seal and Barrier Inspection- Group 4, Completed 10/9/14  
SFP 17, Unit 3 Fire Penetration Seal and Barrier Inspection- Group 9, Completed 12/27/13  
SFP 17, Unit 3 Fire Penetration Seal and Barrier Inspection- Group 9, Completed 12/27/13  
SFP 21, Unit 2 Appendix R Fire Cage Inventory, Completed 11/25/15 SFP 9, Unit 3 - Fire Extinguisher Inspection Data Sheet - Train B, Completed 6/29/16 SFP 9, Unit 3 - Fire Extinguisher Inspection Data Sheet - Train A, Completed 7/11/16  
SFP 21, Unit 2 Appendix R Fire Cage Inventory, Completed 11/25/15  
SFP 9, Unit 3 - Fire Extinguisher Inspection Data Sheet - Train B, Completed 6/29/16  
SFP 9, Unit 3 - Fire Extinguisher Inspection Data Sheet - Train A, Completed 7/11/16  
SFP Procedure 21, Unit 3 Safe Shutdown Fire Cage Inventory, Completed on 11/26/2015  
SFP Procedure 21, Unit 3 Safe Shutdown Fire Cage Inventory, Completed on 11/26/2015  
SP 2402CR, Steam Generator Pressure Rack Instrument Calibration, Revision 0, Completed 8/12/14 and 3/16/16 SP 2601P, Unit 2 CVCS Valve Operability Tests from C-10 and C-02, Revision 0, Completed  
SP 2402CR, Steam Generator Pressure Rack Instrument Calibration, Revision 0, Completed  
10/30/15 SP 2610B, Turbine Driven Auxiliary Feed Pump Operational Tests from C-10, Completed 3/2/16  
8/12/14 and 3/16/16  
SP 2601P, Unit 2 CVCS Valve Operability Tests from C-10 and C-02, Revision 0, Completed  
10/30/15  
SP 2610B, Turbine Driven Auxiliary Feed Pump Operational Tests from C-10, Completed 3/2/16  
SP 2610E, Atmospheric Dump Valve Testing From C-10, C-70A and C-70B, Completed  
SP 2610E, Atmospheric Dump Valve Testing From C-10, C-70A and C-70B, Completed  
10/21/15 SP 2610M, Power Operated Relief Valve Hot Functional Test, Completed 11/1/15 SP 2657, EOP Equipment Inventory, Completed 9/7/15 SP 3442J01, RCS Wide Range Pressure Rack Calibration, Completed 9/16/14 and 2/11/16  
10/21/15  
SP 2610M, Power Operated Relief Valve Hot Functional Test, Completed 11/1/15  
SP 2657, EOP Equipment Inventory, Completed 9/7/15  
SP 3442J01, RCS Wide Range Pressure Rack Calibration, Completed 9/16/14 and 2/11/16  
SP 3444A02, Steam Generator Water Level Wide Range Calibration, Completed 7/10/13 and  
SP 3444A02, Steam Generator Water Level Wide Range Calibration, Completed 7/10/13 and  
3/11/15
3/11/15  
A-7   SP 3451Q01, Unit 3 Instrument Rack Room and Fire Pump House - Halon Fire System Test, Completed 2/26/16 SP 3641B.2, IRR Halon System Flow Test, Completed 5/17/15  
 
A-7  
SP 3451Q01, Unit 3 Instrument Rack Room and Fire Pump House - Halon Fire System Test,  
Completed 2/26/16  
SP 3641B.2, IRR Halon System Flow Test, Completed 5/17/15  
SP 3641B.2, IRR Halon System Flow Test, Completed 5/8/14  
SP 3641B.2, IRR Halon System Flow Test, Completed 5/8/14  
SP 3641D.3, Fire Protection Zone Panel 3B Detector Operability Checks, Completed 1/8/15  
SP 3641D.3, Fire Protection Zone Panel 3B Detector Operability Checks, Completed 1/8/15  
SP 3641D.3, Fire Protection Zone Panel 3B Detector Operability Checks, Completed 1/19/13 SP 3641D.3, Fire Protection Zone Panel 3B Detector Operability Checks, Completed 12/21/14  
SP 3641D.3, Fire Protection Zone Panel 3B Detector Operability Checks, Completed 1/19/13  
SP 3641D.3, Fire Protection Zone Panel 5C EDG A Area Detector Operability Checks, Completed 2/25/16 SP 3641D.5, Fire Damper Operability Verification, Completed 1/25/06  
SP 3641D.3, Fire Protection Zone Panel 3B Detector Operability Checks, Completed 12/21/14  
SP 3641D.5, Fire Damper Operability Verification, Completed 5/8/11 SP 3641D.5, Fire Damper Operability Verification, Completed 9/5/99 SP 3641D.6, Fire Rated Assemblies Inspection, Completed 8/2/15  
SP 3641D.3, Fire Protection Zone Panel 5C EDG A Area Detector Operability Checks,  
SP 3641F.1, Functional Check of the East and West Switchgear Breathing Air System, Completed 6/21/15 SP 3672.2-10, Fire Transfer Switch Panel Operational Testing-3RCS*PCV455A, Completed  
Completed 2/25/16  
11/9/14 SP 3672.2-2, Fire Transfer Switch Panel Operational Testing-3HVP*FN1A and FN1C, Completed 3/20/12 SP 3672.2-7, Fire Transfer Switch Panel Operational Testing-3SWP*MOV54A and MOV54C, Completed 8/1/13 SP 3672.2-8, Fire Transfer Switch Panel Operational Testing-3SWP*MOV71A Completed  
SP 3641D.5, Fire Damper Operability Verification, Completed 1/25/06  
11/23/15 SP 3673.2, Unit 3 Fire Transfer Switch Panel Operational Testing for 3HVP*FN1A and 3HVP*FN1C, Completed 3/20/12 SP 3673.2, Unit 3 Fire Transfer Switch Panel Operational Testing for 3HVR*FN14A, Completed  
SP 3641D.5, Fire Damper Operability Verification, Completed 5/8/11  
10/25/14 SP 3673.2, Unit 3 Fire Transfer Switch Panel Operational Testing for 3HVR*MOD50A, Completed 12/20/12 SP 3673.2, Unit 3 Fire Transfer Switch Panel Operational Testing for 3HVR*ACU1A, Completed  
SP 3641D.5, Fire Damper Operability Verification, Completed 9/5/99  
12/22/15 SP 3673.2, Unit 3 Fire Transfer Switch Panel Operational Testing for 3HVY*FN2A, Completed  
SP 3641D.6, Fire Rated Assemblies Inspection, Completed 8/2/15  
12/18/12 SP 3673.2, Unit 3 Fire Transfer Switch Panel Operational Testing for 3SWP*MOV71A, Completed 11/23/15 SP 3673.4, Auxiliary Shutdown Panel Operability Test for Charging Injection Path, Completed  
SP 3641F.1, Functional Check of the East and West Switchgear Breathing Air System,  
5/1/16 SP 3673.4, Auxiliary Shutdown Panel Operability Test for Charging Isolation Path, Completed  
Completed 6/21/15  
5/1/16 SP 3673.4, Auxiliary Shutdown Panel Operability Test for Train A CVCS Components, Completed 1/14/15 SP 3673.4-001, Auxiliary Shutdown Panel Operability Test, Completed 5/8/16  
SP 3672.2-10, Fire Transfer Switch Panel Operational Testing-3RCS*PCV455A, Completed  
SP 3673.4-004, Auxiliary Shutdown Panel Operability Test Train A Auxiliary Feedwater Components, Completed 2/8/15 SP 3673.4-007, Auxiliary Shutdown Panel Operability Test Train B Auxiliary Feedwater Components, Completed 2/1/15 SP 3673.4-009, Auxiliary Shutdown Panel Operability Test Train B CVCS Components, Completed 5/22/16
11/9/14  
A-8   SP 3673.4-011, Auxiliary Shutdown Panel Operability Test Train A PORV and Block Valves, Completed 1/9/14 SP 3673.4-014, Auxiliary Shutdown Panel Operability Test Non-Train Related Components, Completed 5/1/16 SP2618C, Smoke and Heat Detector Testing, Auxiliary Building, Completed 3/24/16  
SP 3672.2-2, Fire Transfer Switch Panel Operational Testing-3HVP*FN1A and FN1C,  
SP2618C, Smoke Detector Testing, Switchgear Detector Testing, Facility 1, Completed 5/30/16 SP2618C, Smoke Detector Testing, Turbine Building, Completed 1/19/16  SP2618C, Turbine Bldg. 25'6'' Cable Vault and Vertical Shaft Smoke Detector Test, Completed  
Completed 3/20/12  
3/4/16 SP2618D, "A" DG Deluge Systems Design Function Test, Completed 1/12/16   
SP 3672.2-7, Fire Transfer Switch Panel Operational Testing-3SWP*MOV54A and MOV54C,  
Completed 8/1/13  
SP 3672.2-8, Fire Transfer Switch Panel Operational Testing-3SWP*MOV71A Completed  
11/23/15  
SP 3673.2, Unit 3 Fire Transfer Switch Panel Operational Testing for 3HVP*FN1A and  
3HVP*FN1C, Completed 3/20/12  
SP 3673.2, Unit 3 Fire Transfer Switch Panel Operational Testing for 3HVR*FN14A, Completed  
10/25/14  
SP 3673.2, Unit 3 Fire Transfer Switch Panel Operational Testing for 3HVR*MOD50A,  
Completed 12/20/12  
SP 3673.2, Unit 3 Fire Transfer Switch Panel Operational Testing for 3HVR*ACU1A, Completed  
12/22/15  
SP 3673.2, Unit 3 Fire Transfer Switch Panel Operational Testing for 3HVY*FN2A, Completed  
12/18/12  
SP 3673.2, Unit 3 Fire Transfer Switch Panel Operational Testing for 3SWP*MOV71A,  
Completed 11/23/15  
SP 3673.4, Auxiliary Shutdown Panel Operability Test for Charging Injection Path, Completed  
5/1/16  
SP 3673.4, Auxiliary Shutdown Panel Operability Test for Charging Isolation Path, Completed  
5/1/16  
SP 3673.4, Auxiliary Shutdown Panel Operability Test for Train A CVCS Components,  
Completed 1/14/15  
SP 3673.4-001, Auxiliary Shutdown Panel Operability Test, Completed 5/8/16  
SP 3673.4-004, Auxiliary Shutdown Panel Operability Test Train A Auxiliary Feedwater  
Components, Completed 2/8/15  
SP 3673.4-007, Auxiliary Shutdown Panel Operability Test Train B Auxiliary Feedwater  
Components, Completed 2/1/15  
SP 3673.4-009, Auxiliary Shutdown Panel Operability Test Train B CVCS Components,  
Completed 5/22/16  
 
A-8  
SP 3673.4-011, Auxiliary Shutdown Panel Operability Test Train A PORV and Block Valves,  
Completed 1/9/14  
SP 3673.4-014, Auxiliary Shutdown Panel Operability Test Non-Train Related Components,  
Completed 5/1/16  
SP2618C, Smoke and Heat Detector Testing, Auxiliary Building, Completed 3/24/16  
SP2618C, Smoke Detector Testing, Switchgear Detector Testing, Facility 1, Completed 5/30/16  
SP2618C, Smoke Detector Testing, Turbine Building, Completed 1/19/16   
SP2618C, Turbine Bldg. 256 Cable Vault and Vertical Shaft Smoke Detector Test, Completed  
3/4/16  
SP2618D, A DG Deluge Systems Design Function Test, Completed 1/12/16   
SP2618D, Fire Protection System sprinkler and Deluge Design Function test, Completed  
SP2618D, Fire Protection System sprinkler and Deluge Design Function test, Completed  
5/20/15 SP2618H, Fire Protection System Deluge Nozzle Flow Test, Completed 7/16/14  
5/20/15  
SP2618H, Fire Protection System Deluge Nozzle Flow Test, Completed 7/16/14  
SP2618L, Fire Protection Coating Inspection, Completed 8/4/15   
SP2618L, Fire Protection Coating Inspection, Completed 8/4/15   
SP2618L, TSI Fire Wrap Inspection, Completed 8/7/15  
SP2618L, TSI Fire Wrap Inspection, Completed 8/7/15  
SP2657, Inventory Remote Shutdown Station Storage, Completed 5/13/16  
SP2657, Inventory Remote Shutdown Station Storage, Completed 5/13/16  
Operating Experience Evaluations Information Notice 2014-10, Potential Circuit Failure-Induced Secondary Fires or Equipment Damage, dated 9/16/14
   
   
Quality Assurance Audits and Self Assessments Audit 15-04, Fire Protection Program, dated 7/15/15  
Operating Experience Evaluations
 
Information Notice 2014-10, Potential Circuit Failure-Induced Secondary Fires or Equipment
Damage, dated 9/16/14
Quality Assurance Audits and Self Assessments  
Audit 15-04, Fire Protection Program, dated 7/15/15  
   
   
System Health Reports 3341 A, B, C, F - Fire Protections Water, Halon, CO2, Emerg. Breathing Air, dated  10/1/14- 12/31/14 3341 A, B, C, F - Fire Protections Water, Halon, CO2, Emerg. Breathing Air, dated  10/1/15- 12/31/15 3341D - Fire Detection, dated 10/1/14- 12/31/14   
System Health Reports  
3341 A, B, C, F - Fire Protections Water, Halon, CO2, Emerg. Breathing Air, dated   
10/1/14- 12/31/14  
3341 A, B, C, F - Fire Protections Water, Halon, CO2, Emerg. Breathing Air, dated   
10/1/15- 12/31/15  
3341D - Fire Detection, dated 10/1/14- 12/31/14   
3341D - Fire Detection, dated 10/1/15- 12/31/15   
3341D - Fire Detection, dated 10/1/15- 12/31/15   
ELU System Health Report, 1St Quarter 2016
ELU System Health Report, 4th Quarter 2015
Program/Comp Health Report FP- Fire Protection - Including Appendix R, 4th Quarter 2015
Program/Comp Health Report FP- Fire Protection - Including Appendix R, 1st Quarter 2016
System Health Report 2352, 3720B - Safe Shutdown Lighting, 1st Quarter 2016
System Health Report 2352, 3720B - Safe Shutdown Lighting, 4th Quarter 2015
U 2 Fire Protection & Deluge, CO2 Alterex, Halon Supression, 4th Quarter 2014
U 2 Fire Protection & Deluge, CO2 Alterex, Halon Supression, 4th Quarter 2015
Unit 2 AC and DC Systems, 4th qtr. 2015 and 1st Quarter 2016
Unit 3 AC and DC Systems, 4th qtr. 2015 and 1st Quarter 2016


ELU System Health Report, 1
A-9
St Quarter 2016
ELU System Health Report, 4
th Quarter 2015 Program/Comp Health Report FP- Fire Protection - Including Appendix R, 4
th Quarter 2015 Program/Comp Health Report FP- Fire Protection - Including Appendix R, 1
st Quarter 2016 System Health Report 2352, 3720B - Safe Shutdown Lighting, 1
st Quarter 2016 System Health Report 2352, 3720B - Safe Shutdown Lighting, 4
th Quarter 2015 U 2 Fire Protection & Deluge, CO2 Alterex, Halon Supression, 4
th Quarter 2014 U 2 Fire Protection & Deluge, CO2 Alterex, Halon Supression, 4
th Quarter 2015
Unit 2 AC and DC Systems, 4
th qtr. 2015 and 1
st Quarter 2016
Unit 3 AC and DC Systems, 4
th qtr. 2015 and 1
st Quarter 2016
   
   
 
Drawings and Wiring Diagrams  
A-9  Drawings and Wiring Diagrams  
12179-30276, U3 Generator Seal Oil System Emergency Seal Oil pump 3GMO-P2 Control,  
12179-30276, U3 Generator Seal Oil System Em
Revision 5  
ergency Seal Oil pump 3GMO-P2 Control, Revision 5 12179-FIG-77B, Fire Hazard Analysis Plan Elevation 24 Feet 6 inch, Revision 6  
12179-FIG-77B, Fire Hazard Analysis Plan Elevation 24 Feet 6 inch, Revision 6  
12179-FIG-77C, Fire Hazard Analysis Plant Elevation 38 Feet 6 inch, Revision 11  
12179-FIG-77C, Fire Hazard Analysis Plant Elevation 38 Feet 6 inch, Revision 11  
25203-24070, Sheet 10, RCP Oil Collection System Details for RCP Motor in Cubicle "A", Revision 2 25203-24070, Sheet 11, RCP Oil Collection System Details for RCP Motor in Cubicle "A",  dated 5/16/95 25203-24070, Sheet 12, RCP Oil Collection System Details for RCP Motor in Cubicle "A",  dated 4/19/95 25203-24070, Sheet 13, RCP Oil Collection System Details for RCP Motor in Cubicle "A",  dated 4/20/95 25203-28500, Sht.356, Unit 2 PT-1023B Steam Generator Pressure Loop Diagram, Revision 10  
25203-24070, Sheet 10, RCP Oil Collection System Details for RCP Motor in Cubicle A,  
Revision 2  
25203-24070, Sheet 11, RCP Oil Collection System Details for RCP Motor in Cubicle A,   
dated 5/16/95  
25203-24070, Sheet 12, RCP Oil Collection System Details for RCP Motor in Cubicle A,   
dated 4/19/95  
25203-24070, Sheet 13, RCP Oil Collection System Details for RCP Motor in Cubicle A,   
dated 4/20/95  
25203-28500, Sht.356, Unit 2 PT-1023B Steam Generator Pressure Loop Diagram, Revision 10  
25203-30001, Unit 2 Main Single Line Diagram, Revision 40  
25203-30001, Unit 2 Main Single Line Diagram, Revision 40  
25203-30005, Unit 2 Single Line Meter and Relay Diagram 4.16kV Emergency Buses 24C and  
25203-30005, Unit 2 Single Line Meter and Relay Diagram 4.16kV Emergency Buses 24C and  
24D, Revision 21 25203-30009, Unit 2 Single Line Meter and Relay Diagram 4.16kV Emergency Buses 25E and 24G, Revision 13 25203-30022, Sht. 3, Unit 2 DV20 125Vdc and 120Vac Distribution Panel Schedule, Revision  
24D, Revision 21  
21 25203-30023, U2 Single Line Diagram 125VDC System-Turbine Battery, Revision 9 25203-30024, U2 Single Line Diagram 125VDC Emergency & 120VAC Vital Systems, Revision  
25203-30009, Unit 2 Single Line Meter and Relay Diagram 4.16kV Emergency Buses 25E and  
39 25203-30053, Sheet 1, U2 Schematic Diagram 125VDC Switchgear Bus D01, Revision 7  
24G, Revision 13  
25203-30022, Sht. 3, Unit 2 DV20 125Vdc and 120Vac Distribution Panel Schedule, Revision  
21  
25203-30023, U2 Single Line Diagram 125VDC System-Turbine Battery, Revision 9  
25203-30024, U2 Single Line Diagram 125VDC Emergency & 120VAC Vital Systems, Revision  
39  
25203-30053, Sheet 1, U2 Schematic Diagram 125VDC Switchgear Bus D01, Revision 7  
25203-30053, Sheet 3, U2 Schematic Diagram 125VDC Switchgear Bus D02, Revision 9  
25203-30053, Sheet 3, U2 Schematic Diagram 125VDC Switchgear Bus D02, Revision 9  
25203-30053, Sheet 5, U2 Switchgear Diagram 125VDC Switchgear Bus D03, Revision 10  
25203-30053, Sheet 5, U2 Switchgear Diagram 125VDC Switchgear Bus D03, Revision 10  
25203-30102, Unit 2 Instrument Rack Loading Diagram Fire Shutdown Panel C09, Revision 3 25203-32002, Sh. 16, 4.16kV Switchgear Kirk Key Interlocks, Revision 5  
25203-30102, Unit 2 Instrument Rack Loading Diagram Fire Shutdown Panel C09, Revision 3  
25203-32002, Sh. 16, 4.16kV Switchgear Kirk Key Interlocks, Revision 5  
25203-32006, Sheet 13, U2 Magnetic Starter Elementary Diagram, Revision 8  
25203-32006, Sheet 13, U2 Magnetic Starter Elementary Diagram, Revision 8  
25203-32009, Sht. 37, Unit 2 Charging Line Distribution Solenoid Valve CH519, Revision 9  
25203-32009, Sht. 37, Unit 2 Charging Line Distribution Solenoid Valve CH519, Revision 9  
25203-32009, Sht. 41, Unit 2 Charging Pump Control MP18B, Revision 23  
25203-32009, Sht. 41, Unit 2 Charging Pump Control MP18B, Revision 23  
25203-32009, Sht. 42A, Unit 2 Charging Pump Control MP18B, Revision 3 25203-32009, Sht. 6, Unit 2 Volume Control Tank Discharge MOV CH501, Revision 13 25203-34051, Unit 2 Auxiliary Building Miscellaneous Plan Section and Details, Revision 40  
25203-32009, Sht. 42A, Unit 2 Charging Pump Control MP18B, Revision 3  
25203-32009, Sht. 6, Unit 2 Volume Control Tank Discharge MOV CH501, Revision 13  
25203-34051, Unit 2 Auxiliary Building Miscellaneous Plan Section and Details, Revision 40  
25203-39076, Sheet 9A, U2 Magnetic Starter Elementary Diagram, Revision 1  
25203-39076, Sheet 9A, U2 Magnetic Starter Elementary Diagram, Revision 1  
25203-39076, Sheet 9B, U2 Magnetic Starter Elementary Diagram, Revision 1  
25203-39076, Sheet 9B, U2 Magnetic Starter Elementary Diagram, Revision 1  
25203-39220, Sht. 1B, Unit 2 Instrument Rack Loading Diagram Spec 200 Cabinet RC30B, Revision 19 25203-39352, Sheet 1, U2 One Line Diagram, 15KVA Inverter VIP1 & Static Sw. VS1,   
25203-39220, Sht. 1B, Unit 2 Instrument Rack Loading Diagram Spec 200 Cabinet RC30B,  
Revision 5 25203-39353, Sheet 1, U2 One Line Diagram, 15KVA Inverter VIP2 & Static Sw. VS2,   
Revision 19  
Revision 5 25203-39354, Sheet 1, U2 One Line Diagram, 15KVA Inverter VIP3 & Static Sw. VS3,   
25203-39352, Sheet 1, U2 One Line Diagram, 15KVA Inverter VIP1 & Static Sw. VS1,   
Revision 5 25203-39355, Sheet 1, U2 One Line Diagram, 15KVA Inverter VIP4 & Static Sw. VS4, Revision 3 25203-39356, Sheet 1, U2 One Line Diagram, 15KVA Inverter VIP5, Revision 5
Revision 5  
A-10   25203-39357, Sheet 1, U2 One Line Diagram, 15KVA Inverter VIP6, Revision 6 25203-39367, Sheet 6, U2 Schematic Totalizing Box Turbine Battery Charger 201D/DC4, Revision 2 25205-25003, Station Fire Loop Operating & Hydraulic Analysis Schematic, Revision 14  
25203-39353, Sheet 1, U2 One Line Diagram, 15KVA Inverter VIP2 & Static Sw. VS2,   
Revision 5  
25203-39354, Sheet 1, U2 One Line Diagram, 15KVA Inverter VIP3 & Static Sw. VS3,   
Revision 5  
25203-39355, Sheet 1, U2 One Line Diagram, 15KVA Inverter VIP4 & Static Sw. VS4,  
Revision 3  
25203-39356, Sheet 1, U2 One Line Diagram, 15KVA Inverter VIP5, Revision 5  
 
A-10  
25203-39357, Sheet 1, U2 One Line Diagram, 15KVA Inverter VIP6, Revision 6  
25203-39367, Sheet 6, U2 Schematic Totalizing Box Turbine Battery Charger 201D/DC4,  
Revision 2  
25205-25003, Station Fire Loop Operating & Hydraulic Analysis Schematic, Revision 14  
25212-24036, Fire Stop & Seals Map Locations, Revision 0  
25212-24036, Fire Stop & Seals Map Locations, Revision 0  
25212-24037, Fire Stop & Seals Map Locations, Revision 0 25212-24273, Wall Pene. Map Aux. BLDG. EL. 45'-6", Revision 2 25212-29367 SH 20, Fire Protection & Detection Systems, dated 6/2/75  
25212-24037, Fire Stop & Seals Map Locations, Revision 0  
25212-29680 SH.0010, TCO-003 High Density Silicone Elastomer Fire, Air, and/or Radiation Seal for Electrical Blockout Openings, dated 8/20/84 25212-29680 SH.0023, TCO-050 Silicone Foam Fire or Air Seals for Sleeve, Conduit, Cast or Core Bored Openings up to 5" Dial, dated 1/26/85  
25212-24273, Wall Pene. Map Aux. BLDG. EL. 45-6, Revision 2  
25212-29367 SH 20, Fire Protection & Detection Systems, dated 6/2/75  
25212-29680 SH.0010, TCO-003 High Density Silicone Elastomer Fire, Air, and/or Radiation  
Seal for Electrical Blockout Openings, dated 8/20/84  
25212-29680 SH.0023, TCO-050 Silicone Foam Fire or Air Seals for Sleeve, Conduit, Cast or  
Core Bored Openings up to 5 Dial, dated 1/26/85  
25212-30001, Unit 3 Main One Line Diagram, Revision 26  
25212-30001, Unit 3 Main One Line Diagram, Revision 26  
25212-30004, Unit 3 Main One Line Diagram 4160V Normal and Emergency Buses, Revision  
25212-30004, Unit 3 Main One Line Diagram 4160V Normal and Emergency Buses, Revision  
20 25212-30010, Unit 3 6900V One Line Diagram Bus 35A and 35B, Revision 20  
20  
 
25212-30010, Unit 3 6900V One Line Diagram Bus 35A and 35B, Revision 20  
25212-30011, Unit 3 6900V One Line Diagram Bus 35C and 35D, Revision 21 25212-30027, Sht. 3, Unit 3 480V Motor Control Center One Line Diagram Auxiliary Building, Revision 44 25212-30272, Sht. 29A, Unit 3 Feedwater System Steam Generator 3RCS*SG1A Wide Range Level Indication, Revision 8 25212-30272, Sht. 30, Feedwater System Steam Generator 3RCS*SG1A, Revision 5 25212-30343, Sht. 10A, Unit 3 Reactor Coolant System Channel 1 Wide Range Pressure Loop  
25212-30011, Unit 3 6900V One Line Diagram Bus 35C and 35D, Revision 21  
Diagram, Revision 6 25212-30343, Sht. 10B, Unit 3 Reactor Coolant System Channel 1 Wide Range Pressure Loop  
25212-30027, Sht. 3, Unit 3 480V Motor Control Center One Line Diagram Auxiliary Building,  
Diagram, Revision 5 25212-30343, Sht. 10C, Unit 3 Reactor Coolant System Channel 1 Wide Range Pressure Loop  
Revision 44  
Diagram, Revision 5 25212-30343, Sht. 11, Unit 3 Reactor Coolant System Channel 1 Wide Range Pressure Loop  
25212-30272, Sht. 29A, Unit 3 Feedwater System Steam Generator 3RCS*SG1A Wide Range  
Level Indication, Revision 8  
25212-30272, Sht. 30, Feedwater System Steam Generator 3RCS*SG1A, Revision 5  
25212-30343, Sht. 10A, Unit 3 Reactor Coolant System Channel 1 Wide Range Pressure Loop  
Diagram, Revision 6  
25212-30343, Sht. 10B, Unit 3 Reactor Coolant System Channel 1 Wide Range Pressure Loop  
Diagram, Revision 5  
25212-30343, Sht. 10C, Unit 3 Reactor Coolant System Channel 1 Wide Range Pressure Loop  
Diagram, Revision 5  
25212-30343, Sht. 11, Unit 3 Reactor Coolant System Channel 1 Wide Range Pressure Loop  
Diagram, Revision 5  
Diagram, Revision 5  
25212-30379, Sheet 8, U3 Turbine Generator Lube Oil System Emergency Bearing Oil Pump Control, Revision 3 25212-3200, Sht. 7, Elementary Diagram Reactor Head Vent Isolation Valves 3RCS*SV8095A(B), Revision 6 25212-32001, Elementary Diagram 480V MCC Charging Header Isolation Valve 2CHS*MV8438A, Revision 15 25212-32001, Sheet 6CI, U3 Elementary Diagram 125VDC Emergency Bearing Oil Pump [3TML-P1], Revision 10 25212-32001, Sheet 6CS, U3 Elementary Diagram 125VDC Generator Emergency Seal Oil Pump [3GMO-P2], Revision 14 25212-32001, Sht. 7DX, Elementary Diagram Letdown Line Isolation Valves 3RCS*LCV459 and 3RCS*LCV460, Revision 9 25212-32068, U3 Elementary Diagram Diesel Driven Fire Pump M7-7 Control Circuit, Revision  
25212-30379, Sheet 8, U3 Turbine Generator Lube Oil System Emergency Bearing Oil Pump  
2 25212-39002, Sheet 1020, U3 DC Starter Emergency Seal Oil Elementary, Revision D 25212-39002, Sheet 1021, U3 DC Starter Emergency Seal Oil Schematic, Revision C  
Control, Revision 3  
25212-3200, Sht. 7, Elementary Diagram Reactor Head Vent Isolation Valves  
3RCS*SV8095A(B), Revision 6  
25212-32001, Elementary Diagram 480V MCC Charging Header Isolation Valve  
2CHS*MV8438A, Revision 15  
25212-32001, Sheet 6CI, U3 Elementary Diagram 125VDC Emergency Bearing Oil Pump  
[3TML-P1], Revision 10  
25212-32001, Sheet 6CS, U3 Elementary Diagram 125VDC Generator Emergency Seal Oil  
Pump [3GMO-P2], Revision 14  
25212-32001, Sht. 7DX, Elementary Diagram Letdown Line Isolation Valves 3RCS*LCV459 and  
3RCS*LCV460, Revision 9  
25212-32068, U3 Elementary Diagram Diesel Driven Fire Pump M7-7 Control Circuit, Revision  
2  
25212-39002, Sheet 1020, U3 DC Starter Emergency Seal Oil Elementary, Revision D  
25212-39002, Sheet 1021, U3 DC Starter Emergency Seal Oil Schematic, Revision C  
25212-39002, Sheet 1062, U3 Emergency Bearing Oil Pump Starter-Outline Schematic & Conn.  
25212-39002, Sheet 1062, U3 Emergency Bearing Oil Pump Starter-Outline Schematic & Conn.  
Diagram, Revision E
Diagram, Revision E  
A-11   SKE-3.1-ELEC DIST, Emergency System One Line Diagram for Appendix R, Revision 2
 
A-11  
   
   
Piping and Instrumentation Diagrams 25203-26005, Sht. 2, Unit 2 P&ID Feed System, Revision 73  
SKE-3.1-ELEC DIST, Emergency System One Line Diagram for Appendix R, Revision 2
Piping and Instrumentation Diagrams  
25203-26005, Sht. 2, Unit 2 P&ID Feed System, Revision 73  
25203-26008, Sh. 2, Piping and Instrumentation Diagram Service Water, Revision 114  
25203-26008, Sh. 2, Piping and Instrumentation Diagram Service Water, Revision 114  
 
25203-26011, Fire Protection, Revision 57  
25203-26011, Fire Protection, Revision 57 25203-26014, Sht. 1, Unit 2 P&ID Reactor Coolant System, Revision 41 25203-26014, Sht. 2, Unit 2 P&ID Reactor Coolant System, Revision 46  
25203-26014, Sht. 1, Unit 2 P&ID Reactor Coolant System, Revision 41  
25203-26014, Sht. 2, Unit 2 P&ID Reactor Coolant System, Revision 46  
25203-26017, Sht. 1, Unit 2 P&ID Charging System, Revision 63  
25203-26017, Sht. 1, Unit 2 P&ID Charging System, Revision 63  
25212-25008, Yard Water & Fire Protection Piping, Revision 29  
25212-25008, Yard Water & Fire Protection Piping, Revision 29  
 
25212-25009, Yard Water & Fire Protection Piping, Revision 24  
25212-25009, Yard Water & Fire Protection Piping, Revision 24 25212-26902, Sht. 1, Unit 3 P&ID Reactor Coolant System, Revision 33 25212-26902, Sht. 3, Unit 3 P&ID Reactor Coolant System, Revision 25  
25212-26902, Sht. 1, Unit 3 P&ID Reactor Coolant System, Revision 33  
25212-26902, Sht. 3, Unit 3 P&ID Reactor Coolant System, Revision 25  
25212-26904, Sht. 1, Unit 3 P&ID Chemical and Volume Control, Revision 54  
25212-26904, Sht. 1, Unit 3 P&ID Chemical and Volume Control, Revision 54  
25212-26904, Sht. 2, Unit 3 P&ID Chemical and Volume Control, Revision 17  
25212-26904, Sht. 2, Unit 3 P&ID Chemical and Volume Control, Revision 17  
25212-26905, Sht. 1, Unit 3 P&ID Charging Pump Seal and Lubrication, Revision 33  
25212-26905, Sht. 1, Unit 3 P&ID Charging Pump Seal and Lubrication, Revision 33  
25212-26921, Sht. 1, Unit 3 P&ID Component Cooling Water, Revision 33 25212-26970, Fire Protection System, Revision 12  
25212-26921, Sht. 1, Unit 3 P&ID Component Cooling Water, Revision 33  
25212-26970, Fire Protection System, Revision 12  
   
   
Pre-Fire Plans Fire Area AB-6, Auxiliary Building West MCC and Rod Control Area, Revision 0  
Pre-Fire Plans  
Fire Area CB-11, Control Building Instrument Rack Room Underfloor Area, Revision 0 Fire Area EG-3, Emergency Generator North Emergency generator Enclosure, Revision 0 Fire Area ESF-3, Engineered Safety Features Building North Residual Heat Removal Heat  
Fire Area AB-6, Auxiliary Building West MCC and Rod Control Area, Revision 0  
Exchanger Cubicle, Revision 0 MP2 Fire Fighting Strategies, Unit 2, Fire Area A-15, Diesel Generator A Cubicle, Revision 0  
Fire Area CB-11, Control Building Instrument Rack Room Underfloor Area, Revision 0  
MP2 Fire Fighting Strategies, Unit 2, Fire Area A-32, Air Handling Units 38'6'', Revision 0 MP2 Fire Fighting Strategies, Unit 2, Fire Area T-7, 69. And 4.16 KV Switchgear Room, Revision 0 MP2 Fire Fighting Strategies, Unit 2, Fire Area T-9, East 45' Cable Vault (Z1 train), Revision 0  
Fire Area EG-3, Emergency Generator North Emergency generator Enclosure, Revision 0  
 
Fire Area ESF-3, Engineered Safety Features Building North Residual Heat Removal Heat  
Exchanger Cubicle, Revision 0  
MP2 Fire Fighting Strategies, Unit 2, Fire Area A-15, Diesel Generator A Cubicle, Revision 0  
MP2 Fire Fighting Strategies, Unit 2, Fire Area A-32, Air Handling Units 386, Revision 0  
MP2 Fire Fighting Strategies, Unit 2, Fire Area T-7, 69. And 4.16 KV Switchgear Room,  
Revision 0  
MP2 Fire Fighting Strategies, Unit 2, Fire Area T-9, East 45 Cable Vault (Z1 train), Revision 0  
   
   
Fire Drills and Critiques  
Fire Drills and Critiques  
Fire in Building 454, Completed 6/7/16 Fire in U1 Maintenance Shop, Completed 12/14/15 Fire in U2 H2 Seal Oil Skid Pass, Completed 6/18/15  
Fire in Building 454, Completed 6/7/16  
Fire in U1 Maintenance Shop, Completed 12/14/15  
Fire in U2 H2 Seal Oil Skid Pass, Completed 6/18/15  
Fire in U2 Intake, Completed 12/4/15  
Fire in U2 Intake, Completed 12/4/15  
Fire in U2 Lube Oil Room, Completed 6/9/15  
Fire in U2 Lube Oil Room, Completed 6/9/15  
 
Fire in U2 Upper 4160 Switch Gear, Completed 4/28/15  
Fire in U2 Upper 4160 Switch Gear, Completed 4/28/15 Fire in U3 Maintenance Shop, Completed 12/12/15  
Fire in U3 Maintenance Shop, Completed 12/12/15  
   
   
Fire Brigade Training B5b Familiarization PowerPoint Presentation  
Fire Brigade Training  
B5b Familiarization PowerPoint Presentation  
B5b Hands-On Training attendance records, dated 5/12/15 and 11/17/15  
B5b Hands-On Training attendance records, dated 5/12/15 and 11/17/15  
Beyond Design Basis, Non-Licensed Operator Training Presentation  
Beyond Design Basis, Non-Licensed Operator Training Presentation  
   
A-12   Operator Safe Shutdown Training 15605L, EOP 3509.1 Self-Guided in Plant Walkdown, Revision 0 AOP 2559 - Fire AOP 2579A/AA - Appendix R Fire in R-1, Aux Bldg including Control Room/Computer Rooms/25' Cable Vault, Millstone Unit 2 Licensed Operator Training  
Program Slides ASP115C, Auxiliary Shutdown Equipment/Auxiliar
y Shutdown Panel Lesson Plan, Revision 3 C15506N, MP3*NLCT*EOP 3509.1, Revision 0 Common Operating Procedure 200.18 Time Critical Action Validation and Verification Slides, dated 7/12/16 JPM P003, Isolate Emergency Bus 34C in Accordance with EOP 3509.1, Revision 7  
 
JPM P011 (MC-00094), Primary Side Plant Equipment Operator (PEO) Actions on a Control Room Evacuation (Parts 1 and 2), Revision 9/0 JPM P012, Secondary Side PEO Actions on a Control Room Evacuation, Revision 6  
A-12  
Operator Safe Shutdown Training  
15605L, EOP 3509.1 Self-Guided in Plant Walkdown, Revision 0  
AOP 2559 - Fire AOP 2579A/AA - Appendix R Fire in R-1, Aux Bldg including Control  
Room/Computer Rooms/25 Cable Vault, Millstone Unit 2 Licensed Operator Training  
Program Slides  
ASP115C, Auxiliary Shutdown Equipment/Auxiliary Shutdown Panel Lesson Plan, Revision 3  
C15506N, MP3*NLCT*EOP 3509.1, Revision 0  
Common Operating Procedure 200.18 Time Critical Action Validation and Verification Slides,  
dated 7/12/16  
JPM P003, Isolate Emergency Bus 34C in Accordance with EOP 3509.1, Revision 7  
JPM P011 (MC-00094), Primary Side Plant Equipment Operator (PEO) Actions on a Control  
Room Evacuation (Parts 1 and 2), Revision 9/0  
JPM P012, Secondary Side PEO Actions on a Control Room Evacuation, Revision 6  
JPM P015, Secondary Side PEO Actions on a Control Room Evacuation due to Fire, Revision 8  
JPM P015, Secondary Side PEO Actions on a Control Room Evacuation due to Fire, Revision 8  
JPM P173, Aligning the Fire Transfer Switch  
JPM P173, Aligning the Fire Transfer Switch Panel and Auxiliary Shutdown Panel in Response  
Panel and Auxiliary Shutdown Panel in Response  
to a Fire, Revision 2  
to a Fire, Revision 2 JPM P188, Installation of 3CHS-PI102T, Revision 0 JPM P209, Cross-Connect Service Water to East Switchgear Ventilation, Revision 1 SEG S13406L, Respond to a Control Room, Cabl
JPM P188, Installation of 3CHS-PI102T, Revision 0  
e Spreading Area or Instrument Rack Room  
JPM P209, Cross-Connect Service Water to East Switchgear Ventilation, Revision 1  
Fire, Revision 0 SEG S15304L, Fire in Instrument Rack Room, Revision 0  
SEG S13406L, Respond to a Control Room, Cable Spreading Area or Instrument Rack Room  
Fire, Revision 0  
SEG S15304L, Fire in Instrument Rack Room, Revision 0  
Unit 2 Licensed Operator Requalification Program Attendance Sheet for Cycle 16-3, 5/10 - 6/17  
Unit 2 Licensed Operator Requalification Program Attendance Sheet for Cycle 16-3, 5/10 - 6/17  
  Hot Work and Ignition Source Permits, and Tr
   
ansient Combustible Permits and Evaluations  
Hot Work and Ignition Source Permits, and Transient Combustible Permits and Evaluations  
  29633-12-FP 30391-13-IS 31960-15-IS 41224-12-FP  
   
41316-12-FP 41399-12-IS 43879-15-FP 43965-15-IS 44356-16-FP 44385-16-IS 44389-16-IS 44390-16-IS 44499-16-FP  
29633-12-FP  
30391-13-IS  
31960-15-IS  
41224-12-FP  
41316-12-FP  
41399-12-IS  
43879-15-FP  
43965-15-IS  
44356-16-FP  
44385-16-IS  
44389-16-IS  
44390-16-IS  
44499-16-FP  
   
   
Corrective Action Program Documents (Condition Reports)  
Corrective Action Program Documents (Condition Reports)  
  463259 515160 520964 522469 522722 522740 522848 522850 523785 527755 530987 541980  
   
541983 553343 557088 576367  
463259  
578178 578333 581890 582625  
515160  
582652 582665 1004974 1009069 1037462 1041883 1042283* 1043063* 1043417* 1043422* 1043425* 1043455*  
520964  
1043458* 1043959* 1044278* 1044301*  
522469  
1044326* 1044332* 1044334* 1044348*  
522722  
1044422* 1044536* 1044760*   
522740  
  * NRC identified during this inspection.  
522848  
522850  
523785  
527755  
530987  
541980  
541983  
553343  
557088  
576367  
578178  
578333  
581890  
582625  
582652  
582665  
1004974  
1009069  
1037462  
1041883  
1042283*  
1043063*  
1043417*  
1043422*  
1043425*  
1043455*  
1043458*  
1043959*  
1044278*  
1044301*  
1044326*  
1044332*  
1044334*  
1044348*  
1044422*  
1044536*  
1044760*  
   
* NRC identified during this inspection.  


A-13
Work Orders
53M20807693
53012768647
53102490410
53102502011
53102582983
53102605405
53102649190
53102656386
53102659739
53102669361
53102693811
53102695870
53102698825
53102698915
53102698922
53102698928
53102698931
53102716240
53102716256
53102732991
53102735138
53102759052
53102760642
53102764120
53102786767
53102814722
53102846681
53102853315
53102854686
53102861679
53102871440
53102873143
53102887195
53102892290
53102900241
53102905692
53102914238
53102952946
53102958935
   
   
 
Vendor Manuals
A-13  Work Orders
25212-902-001, Vendor Technical Manual for Emergency Lighting from Exide, Holophane,
53M20807693 53012768647 53102490410 53102502011
Dualite, Birns, Revision 6
53102582983 53102605405 53102649190 53102656386
TI 2AI-130, Spec 200 Current-To-Voltage Converters, dated 10/77
53102659739 53102669361 53102693811 53102695870
53102698825 53102698915 53102698922 53102698928 53102698931 53102716240 53102716256 53102732991 53102735138 53102759052 53102760642 53102764120
53102786767 53102814722 53102846681 53102853315
53102854686 53102861679 53102871440 53102873143
53102887195 53102892290 53102900241 53102905692 53102914238 53102952946 53102958935 
   
   
Vendor Manuals 25212-902-001, Vendor Technical Manual for Emergency Lighting from Exide, Holophane, Dualite, Birns, Revision 6 TI 2AI-130, Spec 200 Current-To-Voltage Converters, dated 10/77
Industry Standards  
Industry Standards NFPA 10-1968, Installation for Portable Fire Extinguishers  
NFPA 10-1968, Installation for Portable Fire Extinguishers  
NFPA 13-1971, Installation of Sprinkler Systems  
NFPA 13-1971, Installation of Sprinkler Systems  
NFPA 14-1978, Installation of Standpipe and Hose Systems NFPA 15-1985, Water Spray for Fixed Systems for Fire Protection NFPA 27-1975, Private Fire Brigade  
NFPA 14-1978, Installation of Standpipe and Hose Systems  
NFPA 15-1985, Water Spray for Fixed Systems for Fire Protection  
NFPA 27-1975, Private Fire Brigade  
NFPA 72D-1986, Maintenance and Use of Proprietary protective Signaling Systems  
NFPA 72D-1986, Maintenance and Use of Proprietary protective Signaling Systems  
NFPA 72E-1984, Automatic Fire Detectors  
NFPA 72E-1984, Automatic Fire Detectors  
 
Miscellaneous Documents
Miscellaneous Documents  
Aid Agreement letter Between Millstone and the Waterford Fire Service, dated 8/6/15 Electrical Cable and Conduit Routing Information - SAFE  
Aid Agreement letter Between Millstone and the Waterford Fire Service, dated 8/6/15  
Electrical Cable and Conduit Routing Information - SAFE  
Fire and Hose-Stream tests for Penetration Seal Systems, dated 4/82  
Fire and Hose-Stream tests for Penetration Seal Systems, dated 4/82  
Fire Qualification Test on Floor Penetration Seals, dated 11/30/79  
Fire Qualification Test on Floor Penetration Seals, dated 11/30/79  
Hazard Evaluation Sheet Building - CB, dated 12/11/85 Millstone Site Fire Protection Active Impairment List, dated 7/11/16 Millstone Site Fire Protection Active Impairment List, dated 7/26/16  
Hazard Evaluation Sheet Building - CB, dated 12/11/85  
Millstone Site Fire Protection Active Impairment List, dated 7/11/16  
Millstone Site Fire Protection Active Impairment List, dated 7/26/16  
Millstone Site Fire Protection Active Impairment List, dated 7/27/16  
Millstone Site Fire Protection Active Impairment List, dated 7/27/16  
Waterford Ambulance Service Memorandum of Understanding (MOU), dated 8/5/15  
Waterford Ambulance Service Memorandum of Understanding (MOU), dated 8/5/15  
Waterford Fire Service MOU, dated 8/6/15
Waterford Police Department MOU, dated 9/14/15


Waterford Fire Service MOU, dated 8/6/15 Waterford Police Department MOU, dated 9/14/15
A-14  
LIST OF ACRONYMS
ADAMS
Agencywide Documents Access and Management System
ADV
   
   
 
Atmospheric Dump Valve  
A-14  LIST OF ACRONYMS
AFW   
ADAMS Agencywide Documents Access and Management System ADV  Atmospheric Dump Valve  
Auxiliary Feedwater  
AFW  Auxiliary Feedwater  
AOP  
AOP  Abnormal Operating Procedure BTP  Branch Technical Position CAP  Corrective Action Program  
   
CFR  Code of Federal Regulations  
Abnormal Operating Procedure  
CMEB  Chemical Engineering Branch  
BTP  
 
   
CO 2 Carbon Dioxide CONVEX Connecticut Valley Electric Exchange CR  Condition Report  
Branch Technical Position  
CSD  Cold Shutdown  
CAP  
DC  Direct Current  
   
Dominion Dominion Nuclear Connecticut, Inc.  
Corrective Action Program  
DRS  Division of Reactor Safety EDG  Emergency Diesel Generator EOP  Emergency Operating Procedure  
CFR  
FA  Fire Area  
   
FHA  Fire Hazards Analysis  
Code of Federal Regulations  
FPP  Fire Protection Program FSAR  Final Safety Analysis Report FZ  Fire Zone  
CMEB   
IEEE  Institute of Electrical and Electronics Engineering  
Chemical Engineering Branch  
IMC  Inspection Manual Chapter  
CO2
IP  Inspection Procedure IPEEE  Individual Plant Examination of External Events IR  Inspection Report  
   
LER  Licensee Event Report  
Carbon Dioxide  
LOOP  Loss of Offsite Power  
CONVEX  
Millstone Millstone Power Station Unit 2 and Unit 3  
Connecticut Valley Electric Exchange  
NCV  Non-Cited Violation NFPA  National Fire Protection Association NRC  Nuclear Regulatory Commission  
CR  
OMA  Operator Manual Action  
   
P&ID  Piping and Instrumentation Drawing  
Condition Report  
PARS  Publicly Available Records System RAS  Reasonable Assurance of Safety SBO  Station Blackout  
CSD  
SDP  Significance Determination Process  
   
SER  Safety Evaluation Report  
Cold Shutdown  
SFP  Site Fire Protection  
DC  
SG  Steam Generator UFSAR Updated Final Safety Analysis Report V  Volts  
   
V dc  Voltage Direct Current
Direct Current  
Dominion  
Dominion Nuclear Connecticut, Inc.  
DRS  
   
Division of Reactor Safety  
EDG  
   
Emergency Diesel Generator  
EOP  
   
Emergency Operating Procedure  
FA  
   
Fire Area  
FHA  
   
Fire Hazards Analysis  
FPP  
   
Fire Protection Program  
FSAR   
Final Safety Analysis Report  
FZ  
   
Fire Zone  
IEEE   
Institute of Electrical and Electronics Engineering  
IMC  
   
Inspection Manual Chapter  
IP  
   
Inspection Procedure  
IPEEE   
Individual Plant Examination of External Events  
IR  
   
Inspection Report  
LER  
   
Licensee Event Report  
LOOP   
Loss of Offsite Power  
Millstone  
Millstone Power Station Unit 2 and Unit 3  
NCV  
   
Non-Cited Violation  
NFPA   
National Fire Protection Association  
NRC  
   
Nuclear Regulatory Commission  
OMA   
Operator Manual Action  
P&ID   
Piping and Instrumentation Drawing  
PARS   
Publicly Available Records System  
RAS  
   
Reasonable Assurance of Safety  
SBO  
   
Station Blackout  
SDP  
   
Significance Determination Process  
SER  
   
Safety Evaluation Report  
SFP  
   
Site Fire Protection  
SG  
   
Steam Generator  
UFSAR  
Updated Final Safety Analysis Report  
V  
   
Volts  
V dc  
   
Voltage Direct Current
}}
}}

Latest revision as of 20:18, 9 January 2025

NRC Triennial Fire Protection Inspection Report 05000336/2016007 and 05000423/2016007
ML16258A175
Person / Time
Site: Millstone  Dominion icon.png
Issue date: 09/14/2016
From: Christopher Cahill
Engineering Region 1 Branch 3
To: Heacock D
Dominion Resources
References
IR 2016007
Download: ML16258A175 (37)


See also: IR 05000336/2016007

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION I

2100 RENAISSANCE BLVD.

KING OF PRUSSIA, PA 19406-2713

September 14, 2016

Mr. David A. Heacock

President and Chief Nuclear Officer

Dominion Resources

5000 Dominion Boulevard

Glen Allen, VA 23060-6711

SUBJECT:

MILLSTONE POWER STATION - NRC TRIENNIAL FIRE PROTECTION

INSPECTION REPORT 05000336/2016007 AND 05000423/2016007

Dear Mr. Heacock:

On August 11, 2016, the U.S. Nuclear Regulatory Commission (NRC) completed a triennial fire

protection inspection at Millstone Power Station, Units 2 and 3. The enclosed inspection report

documents the inspection results, which were discussed on August 11, 2016, with Mr. John

Daugherty, Site Vice President - Millstone Power Station, and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commission's rules and regulations, and with the conditions of your

license. The inspectors reviewed selected procedures and records, observed activities, and

interviewed station personnel. The inspectors also reviewed mitigation strategies for addressing

large fires and explosions.

Based on the results of this inspection, one finding of very low safety significance (Green) was

identified. This finding was determined to be a violation of NRC requirements. However,

because of its very low safety significance, and because it was entered into your corrective

action program, the NRC is treating this finding as a non-cited violation (NCV) consistent with

Section 2.3.2 of the NRC Enforcement Policy. If you contest any NCV in this report, you should

provide a written response within 30 days of the date of this inspection report, with the basis for

your denial, to the Nuclear Regulatory Commission, ATTN: Document Control Desk,

Washington D.C. 20555-0001; with copies to the Regional Administrator, Region I; the Director,

Office of Enforcement; and the NRC Resident Inspector at Millstone Power Stations.

D. Heacock

2

In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390 of the NRC's

"Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be

available electronically for public inspection in the NRC Public Document Room or from the

Publicly Available Records System (PARS) component of the NRC's document system,

Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible

from the NRC Web Site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic

Reading Room).

Sincerely,

/RA/

Christopher G. Cahill

Acting Branch Chief

Engineering Branch 3

Division of Reactor Safety

Docket Nos.

50-336, 50-423

License Nos. DPR-65, NPF-49

Enclosure:

Inspection Report 05000336/2016007

and 05000423/2016007

w/Attachment: Supplemental Information

cc w/encl: Distribution via ListServ

ML16258A175

SUNSI Review

Non-Sensitive

Publicly Available

OFFICE

RI/DRS

RI/DRS

RI/DRP

RI/DRS

NAME

JPatel

WCook

GDentel

CCahill

DATE

09/09/16

09/09/16

09/09/16

09/14/16

i

Enclosure

U.S. NUCLEAR REGULATORY COMMISSION

REGION I

Docket Nos.:

50-336, 50-423

License Nos.:

DPR-65, NPF-49

Report Nos.:

05000336/2016007 and 05000423/2016007

Licensee:

Dominion Nuclear Connecticut, Inc.

Facility:

Millstone Power Station, Units 2 and 3

Location:

P.O. Box 128

Waterford, CT 06385

Dates:

July 25, 2016 through August 11, 2016

Inspectors:

J. Patel, Reactor Inspector (Team Leader)

Division of Reactor Safety (DRS)

W. Cook, Senior Reactor Analyst, DRS

E. DiPaolo, Senior Reactor Inspector, DRS

D. Orr, Senior Reactor Inspector, DRS

K. Young, Senior Reactor Inspector, DRS

L. Dumont, Reactor Inspector, DRS

S. Galbreath, Reactor Inspector, DRS

J. Rady, Reactor Inspector, DRS

Observers:

S. Freeman, Senior Reactor Analyst, NRC, Region II, DRS

Approved by:

Chris Cahill, Acting Branch Chief

Engineering Branch 3

Division of Reactor Safety

ii

SUMMARY OF FINDINGS

IR 05000336/2016007, 05000423/2016007; 07/25/2016 - 08/11/2016; Dominion Nuclear

Connecticut, Inc.; Millstone Power Station, Units 2 and 3; Fire Protection (Triennial).

This report covered a two week on-site triennial fire protection team inspection by specialist

inspectors. One finding of very low safety significance was identified. This finding was

determined to be a non-cited violation. The significance of most findings is indicated by their

color (Green, While, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance

Determination Process. The cross-cutting aspects associated with findings were determined

using IMC 0310, "Components Within The Cross-Cutting Areas." Findings for which the

significance determination process (SDP) does not apply may be Green or be assigned a

severity level after NRC management review. The NRC's program for overseeing the safe

operation of commercial nuclear power reactors is described in NUREG-1649, Reactor

Oversight Process, Revision 6, dated July 2016.

Cornerstone: Mitigating Systems

Green. The team identified a finding of very low safety significance (Green) involving a non-

cited violation of Millstone Power Station, Unit 2, Renewed Facility Operating License

Condition 2.C.(3) to implement and maintain in effect all provisions of the approved fire

protection program as described in the Final Safety Analysis Report (FSAR). Specifically,

Dominion failed to maintain the #2 steam generator (SG) atmospheric dump valve (ADV)

free from fire damage, which may have affected the availability to maintain hot shutdown

conditions from the main control room for a fire in Fire Area R-14, Lower 4.16kV Switchgear

Room and Cable Vault. Dominion promptly entered this safe shutdown issue into their

corrective action program as condition report (CR) 1043458. Immediate corrective actions

included implementing compensatory measures in the form of fire watches for fire area R-14

that are being tracked by Reasonable Assurance of Safety (RAS) determination 3037040.

Longer term corrective actions included submitting an exemption request to the NRC for use

of a local operator manual action (OMA) to operate the #2 SG ADV in lieu of meeting fire

protection requirements for fire area R-14. The team considered Dominions immediate and

longer term corrective actions appropriate.

The performance deficiency was more than minor because it affected the Mitigating

Systems cornerstone objective to ensure the availability, reliability, and capability of systems

that respond to an external event to prevent undesirable consequences in the event of a fire.

Specifically, the use of an OMA during post-fire safe shutdown is not as reliable as normal

systems operation which could be utilized had the requirements of 10 CFR Part 50,

Appendix R,Section III.G.2 been met and, therefore, prevented fire damage to credited

components and/or cables, specifically the #2 SG ADV. The inspectors used IMC 0609,

Appendix F, Fire Protection Significance Determination Process, Phase 1 and determined

the reactor is able to reach and maintain a hot safe shutdown condition because the SG

ADVs are used for transition to cold shutdown, therefore this finding was of very low safety

significance (Green). This finding does not have a cross cutting aspect because the

performance deficiency occurred greater than three years ago when the June 30, 2011

exemption request letter to the NRC was supplemented by letter on February 29, 2012, and

is not indicative of current licensee performance. (Section 1R05.01)

iii

Other Findings

Three violations of very low safety significance that were identified by Dominion were reviewed

by the team. Corrective actions taken or planned by Dominion have been entered into

Dominions corrective action program (CAP). The violations and corrective action tracking

numbers are listed in Section 4OA7 of this report.

REPORT DETAILS

Background

This report presents the results of a triennial fire protection inspection conducted in accordance

with the U.S. Nuclear Regulatory Commission (NRC) Inspection Procedure (IP) 71111.05T,

Fire Protection (Triennial). The objective of the inspection was to assess whether Dominion

Nuclear Connecticut, Inc. (Dominion) has implemented an adequate fire protection program

(FPP) and that post-fire safe shutdown capabilities have been established and are being

properly maintained at the Millstone Power Station Unit 2 and Unit 3 (Millstone). The following

fire areas (FA) and/or fire zones (FZ) were selected for detailed review based on risk insights

from the Millstone Individual Plant Examination of External Events (IPEEE).

Unit 2 Fire Areas / Fire Zones

R-7 / A-15, A Diesel Generator Room A

R-1 / A-32, Main Ventilation Room (Air Handling Units)

R-14 / T-7, 6.9 & 4.16 kV Switchgear Room

R-14 / T-9, East Cable Vault

Unit 3 Fire Areas

AB-6, West MCC & Rod Control Area

CB-11, Instrument Rack Room and Underfloor Area

EG-3, North Emergency Generator Enclosure

ESF-3, North Residual Heat Removal - Heat Exchanger Cubicle

Inspection of these areas/zones fulfills the inspection procedure requirement to inspect a

minimum of three samples.

The inspection team evaluated Dominions FPP against applicable requirements which included

Unit 2 Renewed Facility Operating License Condition 2.C.(3), Unit 3 Renewed Facility Operating

License Conditions 2.H, NRC Safety Evaluation Reports (SERs), Title 10 of the Code of Federal

Regulations (10 CFR) 50.48, 10 CFR Part 50, Appendix R and Branch Technical Position (BTP)

Chemical Engineering Branch (CMEB) 9.5-1. The team also reviewed related documents that

included the Updated Final Safety Analysis Report (UFSAR), Fire Protection Program, Fire

Hazards Analyses (FHA), and post-fire Safe Shutdown Analyses Reports.

The team also evaluated two Unit 2 and two Unit 3 licensee mitigating strategies for addressing

large fires and explosions as required by Unit 2 Renewed Facility Operating License Condition

2.C.(13), Unit 3 Renewed Facility Operating License Condition 2.C.(10), and 10 CFR 50.54

(hh)(2). Inspection of these strategies fulfills the inspection procedure requirement to inspect a

minimum of one sample.

Specific documents reviewed by the team are listed in the Attachment to this report.

2

1.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R05 Fire Protection (IP 71111.05T)

.01

Protection of Safe Shutdown Capabilities

a.

Inspection Scope

The team reviewed the FHA, safe shutdown analyses, and supporting drawings and

documentation to verify that post-fire safe shutdown capabilities were properly protected.

The team ensured that applicable separation requirements of Section III.G of 10 CFR

Part 50, Appendix R for Unit 2 and BTP CMEB 9.5-1 for Unit 3 as well as the licensees

design and licensing bases were maintained for the credited safe shutdown equipment

and their supporting power, control, and instrumentation cables. This review included an

assessment of the adequacy of the selected systems for reactivity control, reactor

coolant makeup, reactor heat removal, process monitoring, and associated support

system functions.

b.

Findings

Introduction: The team identified a finding of very low safety significance (Green)

involving a non-cited violation of Millstone Unit 2 Renewed Facility Operating License

Condition 2.C.(3) to implement and maintain in effect all provisions of the approved fire

protection program as described in the FSAR. Specifically, Dominion failed to maintain

the #2 SG ADV free from fire damage, which may have affected the availability to

maintain hot shutdown conditions from the main control room for a fire in Fire Area R-14,

Lower 4.16kV Switchgear Room and Cable Vault.

Description: The inspectors reviewed the operator manual actions (OMAs) contained in

operating procedure AOP 2579M, Fire Procedure for Hot Standby Appendix R Fire Area

R-14, and compared them against the list of NRC approved OMAs in lieu of meeting

III.G.2 fire protection requirements and determined that an unapproved OMA was being

implemented in AOP 2579M. The OMAs in lieu of meeting III.G.2 fire protection

requirements were approved in an NRC exemption dated December 18, 2012. The

missing OMA was an action to locally operate air-operated valve, 2-MS-190B, #2 SG

ADV. The OMA is necessary since a self-induced loss of offsite power (LOOP) will

occur and station blackout (SBO) condition may occur from fire related cable damage.

Either condition, LOOP or SBO, will cause a loss of instrument air in response to a

significant fire in fire area R-14.

The LOOP will occur when AOP 2579M is implemented because step 3.4 requires the

operators to trip the reactor (causing a loss of the normal station service transformer)

and step 3.9 requires the operators to direct CONVEX (transmission operator) to de-

energize the reserve station service transformer. A SBO may subsequently occur if the

B emergency diesel generator (EDG) is running and its output breaker does not close,

3

which could occur due to fire-related circuit damage. In either condition, LOOP or SBO,

the F instrument air compressor, will be de-energized and a loss of instrument air will

occur.

In 2011, Dominion submitted an exemption request to the NRC for several OMAs in lieu

of meeting III.G.2 fire protection requirements in several fire areas and initially postulated

a loss of instrument air for Fire Area R-14. Three OMAs were requested related to the

loss of instrument air for Fire Area R-14 in a June 30, 2011 exemption request letter to

the NRC. Subsequent to the June 30, 2011 exemption request letter, Dominion walked

down several fire areas and from a mechanical perspective concluded that a loss of

instrument air should no longer be postulated for several fire areas. R-14 was included

as a fire area for which a loss of instrument air was no longer considered credible. In a

request for additional information response letter dated February 29, 2012, Dominion

stated that the loss of instrument air was no longer postulated in fire area R-14 and

others, and requested the NRC delete the OMA for locally operating the #2 SG ADV. In

a correction letter dated October 29, 2012, Dominion again reiterated that for Fire Area

R-14, and others, a Loss of Instrument Air was not postulated, but Dominion clarified

that some of the OMAs that were related to a loss of instrument air should be retained

for postulated fire cable damage or loss of power. However, the OMA for locally

operating the #2 SG ADV was not retained since it was not susceptible to cable damage

or loss of power for a fire in area R-14. Dominion stated in its June 30, 2011 exemption

request letter to the NRC that after auxiliary feedwater (AFW) is established from the

control room, operation of the ADV (2-MS-1 90B) is the required method of removing

decay heat to maintain hot standby and transition to cold shutdown.

As described above, the inspectors determined that implementing AOP 2579M as

written will cause a loss of instrument air and the OMA to locally operate the #2 SG ADV

will be necessary after AFW is restored and decay heat removal is transitioned from the

main steam safety valves to the #2 SG ADV for steam generator pressure control. The

inspectors noted that Dominion is currently implementing an unapproved OMA in lieu of

meeting III.G.2 fire protection requirements. Dominion promptly entered this safe

shutdown issue into their corrective action program as CR 1043458. Immediate

corrective actions included implementing compensatory measures in the form of fire

watches for fire area R-14 that are being tracked by RAS determination 3037040.

Longer term corrective actions included submitting an exemption request to the NRC for

use of a local OMA to operate the #2 SG ADV in lieu of meeting fire protection

requirements for fire area R-14. The team considered Dominions immediate and longer

term corrective actions appropriate.

Analysis: Dominions failure to protect the #2 SG ADV, credited for post-fire safe

shutdown from fire damage in Fire Area R-14 caused by single spurious actuation, is

considered a performance deficiency. The performance deficiency was more than minor

because it affected the Mitigating Systems cornerstone objective to ensure the

availability, reliability, and capability of systems that respond to an external event to

prevent undesirable consequences in the event of a fire. Specifically, the use of an

OMA during post-fire safe shutdown may not be as reliable as normal systems operation

which could be utilized had the requirements of 10 CFR Part 50, Appendix R, Section

4

III.G.2 been met and, therefore, prevented fire damage to credited components and/or

cables, specifically the #2 SG ADV.

The inspectors used IMC 0609, Appendix F, Fire Protection Significance Determination

Process, Phase 1 and determined the reactor is able to reach and maintain a hot safe

shutdown condition because the ADVs are used for transition to cold shutdown,

therefore this finding was of very low safety significance (Green).

This finding does not have a cross cutting aspect because the performance deficiency

occurred greater than three years ago when the June 30, 2011 exemption request letter

to the NRC was supplemented by letter on February 29, 2012, and is not indicative of

current licensee performance.

Enforcement: Millstone Power Station, Unit 2, Renewed Facility Operating License

Condition 2.C.(3) requires Dominion in part to implement and maintain in effect all

provisions of the approved fire protection program as described in the FSAR. FSAR

Section 9.10.6, Safety Shutdown Design Bases, states in part Paragraph 50.48(b) of 10

CFR 50, which became effective on February 17, 1981, that all nuclear plants licensed

to operate prior to January 1, 1979, comply with specific portions of Section III of

Appendix R to 10 CFR 50. Section III.G requires that fire protection features be

provided for those systems, structures, and components important to safe shutdown.

These features must be capable of limiting fire damage so that one train of systems

necessary to achieve and maintain hot shutdown conditions from either the main control

room or the emergency control stations is free of fire damage.

Contrary to the above, since February 17, 1981 (the effective date of Appendix R and

revised 10 CFR 50.48), and ongoing as of the inspection exit date, Dominion failed to

implement all provisions of the approved fire protection program. Specifically, the safe

shutdown strategy in Fire Area R-14 for Millstone Unit 2 relied upon an unapproved

OMA to mitigate post-fire safe shutdown equipment malfunctions caused by a single

spurious actuation, in lieu of protecting the equipment in accordance with 10 CFR Part

50 Appendix R,Section III.G.2. The specific OMA associated with Fire Area R-14

includes local manual control of the #2 SG ADV. Dominions immediate corrective

actions included implementing compensatory measure in the form of fire watches for fire

area R-14. Because this violation was of very low safety significance (Green), and was

entered into Dominions CAP (CR 1043458), this issue is being treated as an NCV

consistent with Section 2.3.2 of the Enforcement Policy. (NCV 05000336/2016007-01,

Unapproved OMA in Lieu of Meeting III.G.2 Fire Protection Requirements for Fire

Area R-14, Lower 4kV Switchgear Room and Cable Vault)

.02

Passive Fire Protection

a.

Inspection Scope

The team walked down accessible portions of the selected fire areas to evaluate

whether the material conditions of the fire area boundaries were adequate for the fire

hazards in the area. The team compared the fire area boundaries, including walls,

ceilings, floors, fire doors, fire dampers, penetration seals, and redundant equipment fire

5

barriers to design and licensing basis requirements, industry standards, and the

Millstone Power Station Unit 2 and Unit 3 FPPs, as approved by the NRC, to identify any

potential degradation or non-conformances.

The team reviewed selected engineering evaluations, installation and repair work orders,

and qualification records for a sample of penetration seals to determine whether the fill

material was properly installed and whether the as-left configuration satisfied design

requirements for the intended fire rating.

The team also reviewed recent inspection and functional test records for fire dampers,

and the inspection records for penetration seals and fire barriers, to verify whether the

inspection and testing was adequately conducted, the acceptance criteria were met, and

any potential performance degradation was identified.

b.

Findings

No findings were identified.

.03

Active Fire Protection

a.

Inspection Scope

The team evaluated manual and automatic fire suppression and detection systems in the

selected fire areas to determine whether they were installed, tested, maintained, and

operated in accordance with NRC requirements, National Fire Protection Association

(NFPA) codes of record, and the Millstone FPPs, as approved by the NRC. The team

also assessed whether the suppression systems capabilities were adequate to control

and/or extinguish fires associated with the hazards in the selected areas.

The team reviewed the as-built capability of the fire water supply system to verify the

design and licensing basis and NFPA code of record requirements were satisfied, and to

assess whether those capabilities were adequate for the hazards involved. The team

reviewed the fire water system hydraulic analyses to assess the adequacy of a single

fire water pump to supply the largest single hydraulic load on the fire water system plus

concurrent fire hose usage. The team evaluated the fire pump performance tests to

assess the adequacy of the test acceptance criteria for pump minimum discharge

pressure at the required flow rate, to verify the criteria was adequate to ensure that the

design basis and hydraulic analysis requirements were satisfied. The team also

evaluated the underground fire loop flow tests to verify the tests adequately

demonstrated that the flow distribution circuits were able to meet design basis

requirements. In addition, the team reviewed recent pump and loop flow test results to

verify the testing was adequately conducted, the acceptance criteria were met, and any

potential performance degradation was identified.

The team reviewed initial discharge testing, design specifications, vendor requirements,

modifications and engineering evaluations, and routine functional testing for the CO2 and

Halon suppression systems for the areas protection. The team walked down accessible

potions of the CO2 and Halon systems, including storage tanks and supply systems, to

6

independently assess the material condition, operational lineup, and availability of the

systems. The team also reviewed and walked down the associated firefighting

strategies and CO2 and Halon system operating procedures.

The team walked down accessible portions of the detection and water suppression

systems in the selected areas and major portions of the fire water supply system,

including motor and diesel driven fire pumps, interviewed system and program

engineers, and reviewed selected corrective action program documents (condition

reports) to independently assess the material condition of the systems and components.

In addition, the team reviewed recent test results for the fire detection and suppression

systems for the selected fire areas to verify the testing was adequately conducted, the

acceptance criteria were met, and any performance degradation was identified.

The team assessed the fire brigade capabilities by reviewing training, qualification, and

drill critique records. The team also reviewed Millstone's firefighting strategies (i.e. pre-

fire plans) and smoke removal plans for the selected fire areas to determine if

appropriate information was provided to fire brigade members and plant operators to

identify safe shutdown equipment and instrumentation, and to facilitate suppression of a

fire that could impact post-fire safe shutdown capability. The team independently

inspected the fire brigade equipment, including personnel protective gear (e.g. turnout

gear) and smoke removal equipment, to determine operational readiness for firefighting.

In addition, the team reviewed Millstone's fire brigade equipment inventory and

inspection procedure and recent inspection and inventory results to verify adequate

equipment was available, and any potential material deficiencies were identified.

b.

Findings

No findings were identified.

.04

Protection from Damage from Fire Suppression Activities

a.

Inspection Scope

The team walked down the selected fire areas and adjacent areas, and reviewed

selected documents to determine whether redundant safe shutdown trains could be

potentially damaged from fire suppression activities or from the rupture or inadvertent

operation of fire suppression systems. During the walkdowns, the team evaluated the

adequacy and condition of floor drains, equipment elevations, and spray protection.

Specifically, to determine whether a potential existed to damage redundant safe

shutdown trains, the team evaluated whether:

A fire in one of the selected fire areas would not release smoke, heat, or hot

gases that could cause unintended activation of suppression systems in adjacent

fire areas which could potentially damage all redundant safe shutdown trains; or

A fire suppression system rupture, inadvertent actuation, or actuation due to a

fire, in one of the selected fire areas, could not directly damage all redundant

trains (e.g. sprinkler caused flooding of other than the locally affected train); and

7

Adequate drainage was provided in areas protected by water suppression

systems.

b.

Findings

No findings were identified.

.05

Post-Fire Safe Shutdown Capability - Normal and Alternative

a.

Inspection Scope

The team reviewed the safe shutdown analysis, thermal-hydraulic analysis, operating

procedures, time critical operator action validation studies, piping and instrumentation

drawings (P&lDs), electrical drawings, the UFSAR, and other supporting documents for

the selected fire areas to verify whether Dominion had properly identified the systems

and components necessary to achieve and maintain post-fire safe shutdown conditions.

The team evaluated selected systems and components credited by the safe shutdown

analysis for reactor pressure control, reactivity control, reactor coolant makeup, decay

heat removal, process monitoring, and support system functions to assess the adequacy

of Dominion's alternative shutdown methodology. The team also assessed whether

alternative post-fire shutdown could be performed both with and without the availability

of off-site power. The team walked down selected plant configurations to verify whether

they were consistent with the assumptions and descriptions in the safe shutdown and

fire hazards analyses. In addition, the team evaluated whether the systems and

components credited for use during post-fire safe shutdown would remain free from fire

damage.

The team reviewed the training program for licensed and non-licensed operators to

verify whether it included alternative shutdown capability. The team also verified

whether personnel required for post-fire safe shutdown, using either the normal or

alternative shutdown methods, were trained and available on-site at all times, exclusive

of those assigned as fire brigade members.

The team reviewed the adequacy of procedures utilized for post-fire shutdown and

performed an independent walk through of procedure steps (i.e., a procedure tabletop)

to assess the adequacy of implementation and human factors within the procedures.

The team also evaluated the time required to perform specific actions to verify whether

operators could reasonably be expected to perform those actions within sufficient time to

maintain plant parameters within specified limits.

Specific procedures reviewed for normal and alternative post-fire shutdown included the

following:

Unit 2

AOP 2559, Fire;

AOP 2579A, Fire Procedure for Hot Standby Appendix R Fire Area R-1;

8

AOP 2579AA, Fire Procedure for Cooldown and Cold Shutdown Appendix R Fire

Area R-1;

AOP 2579EE, Fire Procedure for Cooldown and Cold Shutdown Appendix R Fire

Area R-7, R-9, R-14, and R-17;

AOP 2579G, Fire Procedure for Hot Standby Appendix R Fire Area R-7; and,

AOP 2579M, Fire Procedure for Hot Standby Appendix R Fire Area R-14.

Unit 3

EOP 3509, Fire Emergency;

EOP 3509.1, Control Room, Cable Spreading Area or Instrument Rack Room

Fire;

EOP 3509.6, Auxiliary Building West MCC/Rod Control/ACU Area Fire;

EOP 3509.15, North (A) EDG Enclosure or East (A) F.O. Vault Fire; and,

EOP 3509.19, ESF Building North RHR Heat Exchanger Cubicle Fire.

The team reviewed selected operator manual actions to verify whether they had been

properly reviewed and approved and whether the actions could be implemented in

accordance with plant procedures in the time necessary to support the safe shutdown

method for each fire area. The team also reviewed the periodic testing of the alternative

shutdown transfer and isolation capability, and instrumentation and control functions, to

evaluate whether the tests were adequate to ensure the functionality of the alternative

shutdown capability.

b.

Findings

No findings were identified.

.06

Circuit Analysis

a.

Inspection Scope

The team verified that the licensee performed a post-fire safe shutdown analysis for the

selected fire areas and the analysis appropriately identified the structures, systems, and

components important to achieving and maintaining safe shutdown. Additionally, the

team verified that the licensees analysis ensured that necessary electrical circuits were

properly protected and that circuits that could adversely impact safe shutdown due to hot

shorts or shorts to ground were identified, evaluated, and dispositioned to ensure

spurious actuations would not prevent safe shutdown.

The teams review considered fire and cable attributes, cable routing, potential

undesirable consequences and common power supply/bus concerns. Specific items

included the credibility of the fire threat, cable insulation attributes, cable failure modes,

and actuations resulting in flow diversion or loss of coolant events.

The team also reviewed cable raceway drawings and/or cable routing databases for a

sample of components required for post-fire safe shutdown to verify that cables were

9

routed as described in the safe shutdown analysis. The team also reviewed equipment

important to safe shutdown, but not part of the success path, to verify that the licensee

had taken appropriate actions in accordance with the design and licensing basis and

NRC Regulatory Guide 1.189, Revision 2.

Cable failure modes were reviewed for the following components:

Unit 2

P18B, Charging Pump B;

2-CH-501, VCT Outlet Header to Charging Pumps Isolation Valve;

2-CH-519, Loop 1A Charging Isolation Valve; and,

PI-1023B-1, SG #2 Pressure Indicator.

Unit 3

3RCS*LCV459, VCT Letdown Isolation Valve;

3RCS*SV8095A, Head Vent Isolation Valve;

3CHS*MV8438A, Charging Pump A Header Isolation Valve;

3FWS*LI501A, SG #1 Level Indicator; and,

3RCS*PI405B, RCS Pressure Indicator.

The team reviewed a sample of circuit breaker coordination studies to ensure equipment

needed to conduct post-fire safe shutdown activities would not be impacted due to a lack

of coordination that could result in a common power supply or common bus concern.

The team verified that the transfer of control from the control room to the alternative

shutdown location(s) would not be affected by fire-induced circuit faults (e.g. by the

provision of separate fuses and power supplies for alternative shutdown control circuits).

b.

Findings

No findings were identified.

.07

Communications

a.

Inspection Scope

The team reviewed safe shutdown procedures, the safe shutdown analysis, and

associated documents to verify an adequate method of communications would be

available to plant operators following a fire. During this review the team considered the

effects of ambient noise levels, clarity of reception, reliability, and coverage patterns.

The team also inspected the designated emergency storage lockers to verify the

availability of portable radios for the fire brigade and for plant operators. The team also

verified that communications equipment such as repeaters and transmitters would not be

affected by a fire.

10

b.

Findings

No findings were identified.

.08

Emergency Lighting

a.

Inspection Scope

The team observed the placement and coverage area of eight-hour emergency lights

throughout the selected fire areas to evaluate their adequacy for illuminating access and

egress pathways and any equipment requiring local operation or instrumentation

monitoring for post-fire safe shutdown. The team also verified that the battery power

supplies were rated for at least an eight-hour capacity. Preventive maintenance

procedures, the vendor manual, completed surveillance tests, and battery replacement

practices were also reviewed to verify that the emergency lighting was being maintained

consistent with the manufacturers recommendations and in a manner that would ensure

reliable operation.

b.

Findings

No findings were identified.

.09

Cold Shutdown Repairs

a.

Inspection Scope

The team reviewed Dominion's dedicated repair procedures, for components which

might be damaged by fire and were required to achieve post-fire cold shutdown (CSD).

The team evaluated selected CSD repairs to determine whether they could be achieved

within the time frames assumed in the design and licensing bases. In addition, the team

verified whether the necessary repair equipment, tools, and materials (e.g., pre-cut

cables with prepared attachment lugs) were available and accessible on site.

b.

Findings

No findings were identified.

.10

Compensatory Measures

a.

Inspection Scope

The team verified compensatory measures were in place for out-of-service, degraded, or

inoperable fire protection and post-fire safe shutdown equipment, systems, or features

(e.g., detection and suppression systems and equipment, passive fire barriers, pumps,

valves, or electrical devices providing safe shutdown functions or capabilities). The

team evaluated whether the short term compensatory measures adequately

compensated for the degraded function or feature until appropriate corrective action

11

could be taken and that the licensee was effective in returning the equipment to service

in a reasonable period of time.

b.

Findings

No findings were identified.

.11

Fire Protection Program Changes

a.

Inspection Scope

The team reviewed recent changes to the approved fire protection program to verify that

the changes did not constitute an adverse effect on the ability to safely shutdown.

b.

Findings

No findings were identified.

.12

Control of Transient Combustibles and Ignition Sources

a.

Inspection Scope

The team reviewed the licensees procedures and programs for the control of ignition

sources and transient combustibles to assess their effectiveness in preventing fires and

in controlling combustible loading within limits established in the FHA. A sample of hot

work and transient combustible control permits were also reviewed. The team

performed plant walkdowns to verify that transient combustibles and ignition sources

were being implemented in accordance with the administrative controls.

b.

Findings

No findings were identified.

.13

Large Fires and Explosions Mitigation Strategies

a.

Inspection Scope

The team conducted a review of selected mitigation strategies intended to maintain or

restore core decay heat removal and spent fuel pool cooling capabilities under the

circumstances associated with the loss of large areas of the plant due to explosions

and/or fires. The team assessed whether Dominion continued to meet the requirements

of the Millstone Power Station Units 2 and 3 Operating Licenses and 10 CFR

50.54(hh)(2).

The team reviewed the following mitigation strategies:

Unit 2 and 3 Manual Operation of Turbine-Driven AFW Pump; and,

Unit 2 and 3 Manual Operation of SG ADVs.

12

The team's review included: a detailed assessment of the procedural guidance; a

tabletop discussion with licensed operators; and a walk down of four mitigation

strategies with operators to assess the feasibility of the strategies and operator

familiarity; maintenance and surveillance testing of selected strategy equipment; and an

inventory check of the B.5.b pump and equipment trailers to ensure the appropriateness

of equipment storage and availability.

b.

Findings

No findings were identified.

4.

OTHER ACTIVITIES [OA]

4OA2 Identification and Resolution of Problems (IP 71152)

.01

Corrective Actions for Fire Protection Deficiencies

a.

Inspection Scope

The team reviewed a sample of condition reports associated with fire protection program

and post-fire safe shutdown issues to determine whether Millstone was appropriately

identifying, characterizing, and correcting problems in these areas, and to assess

whether the planned or completed corrective actions were appropriate.

b.

Findings

No findings were identified.

4OA3 Follow-up of Events and Notices of Enforcement Discretion (IP 71153)

.1

(Closed) Licensee Event Report (LER) 05000336/2013-003-00 (Unit 2): Postulated DC

Ammeter Circuit Hot Shorts

On October 30, 2013, during a review of industry operating experience, Dominion

identified a postulated fire induced circuit failure involving unfused direct current (DC)

ammeter circuits for Millstone Power Station, Unit 2. The fire induced circuit failures

could cause a secondary fire that could adversely affect safe shutdown equipment and

cause a loss of alternate shutdown capability which is contrary to Unit 2 Renewed

Facility Operating License Condition 2.C.(3) and Appendix R requirements. The license

condition and regulation requires in part, post-fire safe shutdown cables remain free of

the effects of fire-induced cable faults during postulated fires. Specifically, the licensee

identified DC ammeter circuits for Unit 2, were not provided with overcurrent protection

to limit fault current in the 125 volt (V) DC systems. Postulated fires that result in a short

to ground concurrent with an opposite polarity short from the same battery could result in

excessive current flow in the ammeter wiring. The excessive current could heat-up the

conductor and could result in a secondary fire in another fire area. The secondary fire

could adversely affect safe shutdown equipment and cause a loss of alternate shutdown

13

capability. Dominion determined the cause of the condition was a latent design error

that was made during plant construction involving the failure to include protective fuses

in DC ammeter circuits.

The licensee submitted LER 05000336/2013-003-00 to report this event in accordance

with 10 CFR 50.73(a)(2)(ii)(B) as an unanalyzed condition that significantly degraded

plant safety. The licensee entered this issue into their corrective action program as

condition report number CR530987 and implemented compensatory measures in the

affected fire areas pending final resolution of the issue.

The licensee completed an engineering evaluation (RAS000244) of the issue and

developed a design change (MP2-14-01007) to add fuses to the affected ammeter

circuits. Dominion completed the necessary modifications for all affected ammeter

circuits by May 7, 2014.

The significance and enforcement aspect of this issue are discussed in Section 4OA7.1

of this inspection report. LER 05000336/2013-003-00 is closed.

.2

(Closed) Licensee Event Report (LER) 05000336/2014-002-00 (Unit 2): DC Circuit Hot

Shorts

On March 12, 2014, during a review of industry operating experience, Dominion

identified postulated fire induced circuit failures involving unfused DC motor control

circuits for Millstone Power Station Unit 2. The postulated fire induced circuit failures

could cause a secondary fire that could adversely affect fire safe shutdown equipment

contrary to Unit 2 Renewed Facility Operating License Condition 2.C.(3) and Appendix

R requirements. The license condition and regulation requires in part, post-fire safe

shutdown cables remain free of the effects of fire induced cable faults during postulated

fires. Specifically, the licensee identified 125 V DC control and indication circuits for a

non-safety related main turbine emergency lube oil pump that was not provided with

overcurrent protection. Postulated fires in the turbine battery room, the cable vault, the

plant equipment operator meeting area and the control room could cause failure of the

unprotected 125 V DC circuits, which in turn could cause failure of the control circuits for

safe shutdown equipment. Dominion determined the cause of the condition was a

manufacturers design error that involved the failure to include protective fuses in DC

motor control circuits during plant construction.

The licensee submitted LER 05000336/2014-002-00 (Unit 2) to report this event in

accordance with 10 CFR 50.73(a)(2)(ii)(B) as an unanalyzed condition that significantly

degraded plant safety. The licensee entered this issue into their corrective action

program as condition report number CR541980 and implemented compensatory

measures in the affected fire areas pending final resolution of the issue.

The licensee completed an engineering evaluation (RAS000252) of the issue and

developed a design change (MP2-14-01040) to add overcurrent protection (fuses) to

the affected motor control circuit. Dominion completed the necessary modifications for

the affected motor control circuit by May 5, 2014.

14

The significance and enforcement aspect of this issue are discussed in Section 4OA7.2

of this inspection report. LER 05000336/2014-002-00 (Unit 2) is closed.

.3

(Closed) Licensee Event Report (LER) 05000423/2014-002-00 (Unit 3): DC Circuit Hot

Shorts

On March 12, 2014, during a review of industry operating experience, Dominion

identified postulated fire induced circuit failures involving unfused DC motor control

circuits for Millstone Power Station Unit 3. The postulated fire induced circuit

failures could cause a secondary fire that could adversely affect fire safe shutdown

equipment contrary to Unit 3 Renewed Facility Operating License Condition 2.H

and the branch technical condition (BTP) 9.5-1 requirements. The license

condition and the BTP requires in part, post-fire safe shutdown cables remain free

of the effects of fire-induced cable faults during postulated fires. Specifically, the

licensee identified 125 V DC control circuits for non-safety related main turbine

emergency lube oil and a main generator emergency seal oil pumps that were not

provided with overcurrent protection. Postulated fires in the turbine battery

switchgear area, the cable spreading room, the instrument rack room, and the

control room could cause failure of the unprotected 125 V DC control circuits,

which in turn could cause failure of control circuits for safe shutdown equipment.

Dominion determined the cause of the condition was a manufacturers design

error that involved the failure to include protective fuses in DC motor control

circuits during plant construction.

The licensee submitted LER 05000423/2014-002-00 (Unit 3) to report this event in

accordance with 10 CFR 50.73(a)(2)(ii)(B) as an unanalyzed condition that significantly

degraded plant safety. The licensee entered this issue into their corrective action

program as condition report number CR541983 and implemented compensatory

measures in the affected fire areas pending final resolution of the issue.

The licensee completed an engineering evaluation (RAS000253) of the issue and

developed design change modifications (MP3-14-01071 and MP3-14-01092) to add

overcurrent protection (fuses) to the affected motor control circuits. Dominion completed

the necessary modifications for all affected motor control circuits by November 2, 2014.

The significance and enforcement aspect of this issue are discussed in Section 4OA7.3

of this inspection report. LER 05000289/2014-001-00 (Unit 3) is closed.

15

4OA6 Meetings, Including Exit

Exit Meeting Summary

The team presented the inspection results to Mr. John Daugherty, Site Vice President,

Millstone Power Station, and other members of the site staff at an exit meeting on

August 11, 2016. No proprietary information was included in this inspection report.

4OA7 Licensee-Identified Violations

The following violations of very low safety significance (Green) were identified by the

licensee and are violations of NRC requirements. These issues satisfy the criteria of the

NRC Enforcement Policy of being dispositioned as Non-Cited Violations.

.1

LER 05000336/2013-003-00 (Unit 2) describes an unanalyzed condition in which

Dominion identified their DC ammeter circuits were unfused. Specifically, Dominion did

not provide overcurrent protection for wiring associated with DC ammeter indication in

the control room to prevent wires from overheating due to fire induced faults and

excessive currents flowing through the cable. With enough current flowing through the

cable, the potential existed that the overloaded ammeter wiring could damage system

wiring or adjacent safety-related circuits in the cable raceways needed for post-fire safe

shutdown. This condition could result in a loss of the associated safe shutdown

components or a secondary fire in another fire area. The failure to protect safe

shutdown cables from the effects of postulated fires was a performance deficiency.

This performance deficiency was a violation of Millstone Power Station, Unit 2, Renewed

Facility Operating License Condition 2.C.(3), which requires in part, post-fire safe

shutdown cables remain free of the effects of fire-induced cable faults during postulated

fires. Contrary to the above, Dominion identified they failed to meet this requirement and

the condition existed since initial construction of Unit 2. The issue was more than minor

because it was associated with the protection against external events (fire) attribute of

the mitigating systems cornerstone and it adversely affected the cornerstone objective of

ensuring the availability, reliability, and capability of systems that respond to initiating

events to prevent undesirable consequences. The team determined that the finding was

of very low safety significance (Green), based IMC 0609, Appendix F, Fire Protection

Significance Determination Process (SDP), Phase 2 screening criteria.

The finding screened to Green based upon, task number 2.3.5, because the

affected cables were routed in alternate shutdown fire areas that are continually

manned or protected by detection and automatic suppression systems.

Remaining fire areas are protected by detection systems, automatic suppression

systems or rely on manual fire-fighting activities. Additionally, the cable

construction is Institute of Electrical and Electronics Engineers (IEEE) 383

(thermoset) which decreases the likelihood of inter-cable and intra-cable

interactions. Based on a team walkdown, the team determined that the ammeter

cable routing was not routed near a credible fire ignition source in the affected

fire areas. Because this finding is of very low safety significance and had been

entered into Dominions corrective action program (CR530987), this violation is

16

being treated as a Green, licensee-identified NCV consistent with the NRCs

Enforcement Policy.

.2

LER 05000336/2014-002-00 (Unit 2) describes an unanalyzed condition in which

Dominion identified DC motor control circuits were unfused. Specifically,

Dominion did not provide overcurrent protection for wiring associated with 125 V

DC control circuits for a non-safety related main turbine emergency lube oil pump

to prevent wires from overheating due to fire induced faults and excessive

currents flowing through the cable. With enough current flowing through the

cable, the potential existed that the overloaded motor control wiring could damage

adjacent control circuit wiring for components which are needed to achieve and

maintain post-fire safe shutdown for a fire in several fire areas (turbine battery

room, cable vault, plant equipment operator meeting area, control room). This

condition could result in a loss of the associated safe shutdown components or a

secondary fire in another fire area. The failure to protect safe shutdown cables

from the effect of postulated fires was a performance deficiency.

This performance deficiency was a violation of Millstone Power Station, Unit 2,

Renewed Facility Operating License Condition 2.C.(3), which requires, in part, post-fire

safe shutdown cables remain free of the effects of fire induced cable faults during

postulated fires. Contrary to the above, Dominion identified they failed to meet this

requirement and the condition existed since initial construction. The issue was more

than minor because it was associated with the protection against external events (fire)

attribute of the mitigating systems cornerstone and it adversely affected the

cornerstone objective of ensuring the availability, reliability, and capability of systems

that respond to initiating events to prevent undesirable consequences. The team

determined that the finding was of very low safety significance (Green), based on IMC 0609, Appendix F, Fire Protection Significance Determination Process, Phase 2

screening criteria.

The finding screened to Green based upon, task number 2.3.5, because the affected

cables were routed in alternate shutdown fire areas that are continually manned or

protected by detection and automatic suppression systems. Remaining fire areas are

protected by detection systems, automatic suppression systems or rely on manual fire-

fighting activities. Additionally, the cable construction is IEEE 383 (thermoset) which

decreases the likelihood of inter-cable and intra-cable interactions. Based on a team

walkdown, the team determined that the main turbine emergency lube oil pump cable

routing was not routed near a credible fire ignition source in the affected fire areas.

Because this finding is of very low safety significance and had been entered into

Dominions corrective action program (CR541980), this violation is being treated as a

Green, licensee-identified NCV consistent with the NRCs Enforcement Policy.

.3

LER 05000423/2014-002-00 (Unit 3) describes an unanalyzed condition in which

Dominion identified DC motor control circuits were unfused. Specifically, Dominion did

not provide overcurrent protection for wiring associated with 125 V DC control circuits for

non-safety related main turbine emergency lube oil and main generator emergency seal

oil pumps to prevent wires from overheating due to fire induced faults and excessive

currents flowing through the cable. With enough current flowing through the cable, the

17

potential existed that the overloaded motor control wiring could damage adjacent control

circuit wiring for components which are needed to achieve and maintain post-fire safe

shutdown for a fire in several fire areas (turbine battery switchgear area, cable spreading

room, instrument rack room, control room). This condition could result in a loss of the

associated safe shutdown components or a secondary fire in another fire area. The

failure to protect safe shutdown cables from the effect of postulated fires was a

performance deficiency.

This performance deficiency was a violation of Millstone Power Station, Unit 3,

Renewed Facility Operating License Condition 2.H, which requires, in part, post-fire

safe shutdown cables remain free of the effects of fire induced cable faults during

postulated fires. Contrary to the above, Dominion identified they failed to meet this

requirement and the condition existed since initial construction. The issue was more

than minor because it was associated with the protection against external events (fire)

attribute of the mitigating systems cornerstone and it adversely affected the

cornerstone objective of ensuring the availability, reliability, and capability of systems

that respond to initiating events to prevent undesirable consequences. The team

determined that the finding was of very low safety significance (Green), based on IMC 0609, Appendix F, Fire Protection Significance Determination Process, Phase 2

screening criteria.

The finding screened to Green based upon, task number 2.3.5, because the affected

cables were routed in alternate shutdown fire areas that are continually manned or

protected by detection and automatic suppression systems. Remaining fire areas are

protected by detection systems, automatic suppression systems or rely on manual fire-

fighting activities. Additionally, the cable construction is IEEE 383 (thermoset) which

decreases the likelihood of inter-cable and intra-cable interactions. Based on a team

walkdown, the team determined that the main turbine emergency lube oil and main

generator emergency seal oil pump cable routing was not routed near a credible fire

ignition source in the affected fire areas. Because this finding is of very low safety

significance and had been entered into Dominions corrective action program

(CR541983), this violation is being treated as a Green, licensee-identified NCV

consistent with the NRCs Enforcement Policy.

ATTACHMENT: SUPPLEMENTAL INFORMATION

A-1

Attachment

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

J. Daugherty, Site Vice President

D. Blakeney, Assistant Plant Manager

P. Anastas, Safe Shutdown Engineer

J. Armstrong, Fire Protection Engineer

T. Bryant, Maintenance Supervisor

D. DelBiondo, Site Fire Marshal

J. Farley, Electrical System Engineer

B. Ferguson, Unit 2 Senior Reactor Operator

R. Garver, Engineering Director

L. Kelly, Engineering Lead

W. McCollum, Unit 2 Supervisor

D. Mello, Senior Fire Instructor

K. Perkins, Electrical Engineering Supervisor

P. Russell, Unit 3 Senior Reactor Operator

A. Vargas-Mendez, Licensing Engineer

NRC Personnel

C. Cahill, Acting Branch Chief, Engineering Brach 3, Division of Reactor Safety

C. Highley, Resident Inspector, Millstone Power Station

L. Mckown, Resident Inspector, Millstone Power Station

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

None

Opened and Closed 05000336/2016007-01

NCV

Unapproved OMA in Lieu of Meeting III.G.2 Fire

Protection Requirements for Fire Area R-14, Lower

4kV Switchgear Room and Cable Vault

Closed

05000336/2013-003-00

LER

Postulated DC Ammeter Circuit Hot Shorts (Unit 2),

(Section 4OA3.1)

05000336/2014-002-00

LER

DC Circuit Hot Shorts (Unit 2), (Section 4OA3.2)

05000423/2014-002-00

LER

DC Circuit Hot Shorts (Unit 3), (Section 4OA3.3)

Discussed

None

A-2

LIST OF DOCUMENTS REVIEWED

Fire Protection Licensing Documents

25203-SP-M2-SU-1046, Unit 2 Appendix R Compliance Report, Revision 1

25212-BTP-9.5-1, Unit 3 Branch Technical Position 9.5-1 Compliance Report, Revision 4

25212-MP3-SFR, Millstone Power Station, Unit 3, Safety Function Requirement Manual,

Revision 6

LBDCR 07-MP2-010, Millstone U2 Technical Requirements, dated 10/5/09

Letter from Dominion to NRC, Dominion Nuclear Connecticut, Inc. Millstone Power Station Unit

2 Response to Request for Additional Information Request for Exemption from

10 CFR 50, Appendix R, Section III.G., Fire Protection of Safe Shutdown Capability, with

Attachment, dated 2/29/12

Letter from Dominion to NRC, Dominion Nuclear Connecticut, Inc. Millstone Power Station Unit

2 Request for a Revision of an Exemption from 10 CFR 50, Appendix R, Section III.G.,

Fire Protection of Safe Shutdown Capability, with Attachment, dated 10/29/12

Letter from Dominion to NRC, Dominion Nuclear Connecticut. Inc. Millstone Power Station Unit

2 Request for Exemption from 10 CFR 50. Appendix R.Section III.G., Fire Protection of

Safe Shutdown Capability, with Attachments, dated 6/30/11

Letter from NRC to Dominion, Millstone Power Station, Unit 2 -Correction to Previously Issued

Exemption from the Requirements of 10 CFR Part 50, Appendix R, Section III.G.2.

(TAC No. ME6693) with Enclosure, dated 12/18/12

Millstone Unit 2 Technical Requirement Manual, Section 3/4.7.9, Fire Protection System, 2/2/10

Millstone Unit 3 Fire Protection Evaluation Report, Revision 17.4

MP-SPEC-ENG-BTP-9.5-1, Millstone Unit 3 Branch Technical Position (BTP) 9.5-1 Compliance

Report, Revision 4

U2-24-FPP-FHA, Unit 2 Fire Hazards Analysis, Revision 12

Updated Final Safety Analysis Report, Section 9.5.1, Fire Protection System, Revision 28.2

Design Basis Documents

Fire Code Compliance Review of Safety Related Areas - Fire Protection Systems -Fire

Alarm/Detection Systems and the plants Fire Pumps, dated 9/86

TR-151, Fire and Hose Stream Test of #TCO-003 High Density Silicone Elastomer used in Elec.

Opening, Revision 0

TR-189, Fire and Hose Stream Test of 6, 8, and 10 thick specimens of TCO-050, Revision 1

Design Changes

DCN DM3-00-1286-97, Revision to the BTP 9.5-1 Compliance Report to Include RHS MOVs,

dated 2/5/98

DCR M2-97034, Thermo-Lag Modifications for MP2, Revision 0

M2-98095, TDAFWP Redundant Power Supply, Revision 0

MP2-14-01007, DC Ammeter Hot Short Modification, Revision 1

MP2-14-01040, Appendix R Hot Short Circuit Modification for Emergency Bearing Oil Pump

P63, Revision 1

MP3-13-01183, RHR Cross-Train Suction Motor-Operated Valve Breaker Normal Alignment

Change, dated 10/29/13

MP3-14-01071, Appendix R Hot Short Circuit Modification for Emergency Bearing Oil Pump

3TML-P1, Revision 0

A-3

MP3-14-01092, Appendix R Hot Short Circuit Modification for Emergency Seal Oil Pump

3GMO-P2, Revision 0

MP3-14-01187, MP3 RPCCW Heat Exchanger 3CCP*E1B Replacement, dated 7/6/15

MPG-13-01131, MDM Flex Strategy Support Modification, dated 9/16/14

Calculations/Engineering Evaluation Reports

25203-ER-98-0151, Fire Test Performed for Florida Power & Light Company for Electrical

Raceways Protected with Thermo-Lag Fire Barrier Systems, Revision, 0

25203-ER-99-0092, Millstone Unit 2 Appendix R Cooldown Analysis Assumptions and Results,

Revision 3

97-ENG-01912E2, 4.16kV Switchgear Relay Settings, Revision 0

98-ENG-02411-C2, MP2 Evaluation Flooding Outside Containment, Revision 1

98-ENG-02621-M2, Determination of the Instrument Air Requirement for Certain Safety Related

Valves, Revision 3 99-026, Calculation Change Notice No. 1, Millstone Site Fire Loop Flow Model Bench Markings,

Revision 1 99-026, Calculation Change Notice No. 3, Millstone Site Fire Loop Flow Model Bench Markings,

Revision 1 99-026, Calculation Change Notice No. 4, Millstone Site Fire Loop Flow Model Bench Markings,

Revision 1 99-026, Millstone Site Fire Loop Flow Model Bench Markings, Revision 1

DNC 2512-ER-04-0030, Validation and Verification of EOP 3509.1 Using Simulator, Field and

Table Top Validation, dated 5/28/04

EMP-186, Millstone Nuclear Power Plant U2 Combustible Loading Re-Analysis Calculation,

Revision 2

ER-97-0295, Sound Powered Phone and Trunked Radio Systems - Cable Selection, Routing

and Figures, dated 1/16/98

ER-97-0302, MP3 BTP 9.5-1 Compliance Report Section 6.2 Revision - Communication

Systems, dated 2/10/98

M2-EV-98-0113, Technical Evaluation for 120Vac Vital Bus Appendix R Coordination Study,

Revision 1

M3-EV-98-0011, Technical Evaluation for The Use of an 800 MHz Carrier Frequency Trunked

Radio System at Millstone Unit 3 for General Purposes and Appendix R Requirements,

Revision 1

MP-CALC-ENG-S-0426535, MP3 BTP 9.5-1 RELAP5 Fire Shutdown Analysis 3650 and 3725

MWt, Revision 2

P1164-MP2-COORD, Unit 2 Breaker/Fuse Coordination for the Appendix R Circuits, Revision 0

RAS000244, Postulated DC Ammeter Circuit Hot Shorts, Revision 0

RAS000252, DC Circuit Hot Shorts, Revision 0

RAS000253, DC Circuit Hot Shorts, Revision 0

S-02824S2, Millstone Unit 2, R-2 Fire, Appendix R Analysis, Revision 2

SP-M3-EE-269, Unit 3 Electrical Design Criteria, Revision 3

W2-517-744-RE, MP2 Appendix R Cooldown, Revision 3

A-4

Procedures

3783EA, Component Cooling Pump Motor Replacement for Fire Protection, Revision 005-02

C MP 790, Emergency Light Inspection and Testing, Revision 004-02

C OP 200.18, Time Critical Action Validation and Verification, Revision 2

C OP 200.18, Time Critical Action Validation and Verification, Revision 3

C SP 600.24, Fire Brigade Equipment Inspection, Revision 000-04

C SP 600.28, Fire Brigade vehicle Equipment Inspection Data Sheet (R3), Revision 000-05

C SP600.24, Unit 2 Fire Brigade Equipment Inspection, Revision 001-00

CM-AA-ETE-101, Engineering Technical Evaluation (ETE), Revision 6

CM-AA-FPA-10, Fire Protection/Appendix R (Fire Safe Shutdown) Program, Revision 2

CM-AA-FPA-100, Fire Protection/Appendix R (Fire Safe Shutdown) Program, Revision 11

CM-AA-FPA-101, Control of Combustible and Flammable Materials, Revision 8

CM-AA-FPA-102, Fire Protection and Fire Safe Shutdown review and preparation Process and

Preparation Process and Design Change Process, Revision 6

COM-04-C, Plant Communication Systems, Revision 0

ER-AA-102, Preventive Maintenance Program, Revision 9

ER-AA-MRL-100, Implementing Maintenance Rule, Revision 10

FB-00012, Self-Contained Breathing Apparatus SCOTT 4.5, Revision 7

MP 2720U1, Cold Shutdown Fire Damage Repair Procedure for Fire Area R-1 (Appendix R),

Revision 004-02

SA-AA-115, Conduct of Fire Drills, Revision 2

SFP 10, Fire Protection Inspections, Revision 005-03

SFP 21, Appendix R Fire Cage Inventory, Revision 002-06

SP 2402CR, Steam Generator Pressure Rack Instrument Calibration, Revision 0

SP 2601P, CVCS Valve Operability Tests From C-10 and C-02, Revision 0

SP 2610B, Turbine Driven Auxiliary Feed Pump Operational Tests from C-10, Revision 1

SP 2610E, Atmospheric Dump Valve Testing from C-10, C-70A and C-70B, Revision 1

SP 2610M, Power Operated Relief Valve Hot Functional Test, Revision 0

SP 3442J01, RCS Wide Range Pressure Rack Calibration, Revision 7

SP 3444A02, Steam Generator Water Level Wide Range Calibration, Revision 7

SP 3641D.3, Fire Detection and Control System Operability Check, Revision 015

SP 3641D.5, Fire Damper Operability Verification, Revision 012

SP 3641F.1, Functional Check of the East and West Switchgear Breathing Air Systems,

Revision 2

SP 3673.2, Fire Transfer Switch Panel Operational Testing, Revision 002-06

SP 3673.4, Auxiliary Shutdown Panel Operability Test, Revision 010

TR-MP-TPG-2300, Fire Protection Programs Training Program Guide (TPG), Revision 2

WC5, Fuse Control, Revision 2

Operations Procedures

AOP 2559, Millstone Unit 2 Fire, Revision 10

AOP 2559, Procedure Basis Document, Fire, Revision 009-00

AOP 2579A, Fire Procedure for Hot Standby Appendix R Fire Area R-1, Revision 011-00

AOP 2579A, Procedure Basis Document, Fire Procedure for Hot Standby Appendix R Fire Area

R-1, Revision 011-00

AOP 2579A, Unit 2 Fire Procedure for Hot Standby Appendix R Fire Area R-1, Revision 11

AOP 2579AA, Fire Procedure for Cooldown and Cold Shutdown, Appendix R Fire Area R-1,

Revision 004-08

A-5

AOP 2579EE, Fire Procedure for Cooldown and Cold Shutdown, Appendix R Fire Area R-7, R-

9, R-14, and R-17, Revision 005-09

AOP 2579G, Fire Procedure for Hot Standby Appendix R Fire Area R-7, Revision 006-10

AOP 2579M, Fire Procedure for Hot Standby Appendix R Fire Area R-14, Revision 006-06

AOP 3577, Loss of Normal and Offsite Power to a 4.16 kV Emergency Bus, Revision 003

AOP 3577, Procedure Basis Document, Loss of Normal and Offsite Power to a 4.16 kV

Emergency Bus, Revision 002-00

AOP 3581, Immediate Operator Actions, Revision 003

COP 200.2AIR, Airborne Threat, Revision 002-03

EDMG 2.01, MP2 B.5.b Event Control Room Response, Revision 004

EDMG 2.02, MP2 B.5.b Event TSC Response, Revision 010

EOP 2540, Functional Recovery, Revision 025-00

EOP 2540D, Functional Recovery of Heat Removal, Revision 022-00

EOP 2541, Appendix 36, ADV Local Operation, Revision 000-02

EOP 2541, Appendix 7, TDAFW Pump Abnormal Startup, Revision 000-01

EOP 2541, Standard Appendices, Revision 006

EOP 35 GA-31, Locally Restoring AFW Flow, Revision 004

EOP 3509, Fire Emergency, Revision 027-00

EOP 3509, Procedure Basis Document, Fire Emergency, Revision 026-00

EOP 3509.1, Control Room, Cable Spreading Area or Instrument Rack Room Fire,

Revision 019-00

EOP 3509.1, Procedure Basis Document, Control Room, Cable Spreading Area or Instrument

Rack Room Fire, Revision 019-00

EOP 3509.15, North (A) EDG Enclosure or East (A) F.O. Vault Fire, Revision 001

EOP 3509.15, Procedure Basis Document, North (A) EDG Enclosure or East (A) F.O. Vault

Fire, Revision 001

EOP 3509.19, ESF Building North RHR Heat Exchanger Cubicle Fire, Revision 000-01

EOP 3509.19, Procedure Basis Document, ESF Building North RHR Heat Exchanger Cubicle

Fire, Revision 000-01

EOP 3509.6, Auxiliary Building West MCC/Rod Control/ACU Area Fire, Revision 002-01

EOP 3509.6, Procedure Basis Document, Auxiliary Building West MCC/Rod Control/ACU Area

Fire, Revision 002-01

MP-PROC-OPS-OP-2322, Auxiliary Feedwater System, Revision 029

OP 2343, 4160 Volt Electrical System, Revision 022

OP 3341B, Fire Protection Halon System, Revision 005-06

OP 3353.MB4A, Main Board 4A Annunciator Response, Revision 003

OP 3353.MB4B, Main Board 4B Annunciator Response, Revision 005

OP-3322, Auxiliary Feedwater System, Revision 025

SACRG-3, Severe Accident CR Guideline for MP3 B.5.b Initial Event Response, Revision 004

SAG-1, Injection into the Steam Generators, Revision 011

SAG-2, Depressurize the RCS, Revision 003

SAG-9, MP3 B.5.b Event TSC Response (EDMG), Revision 016

SP 2669A, Unit 2 Auxiliary Building Rounds, Revision 063

A-6

Completed Tests/Surveillances

722481, B.5.b pump annual preventive maintenance, Completed 7/26/16

C OP 200.18, Time Critical Action Validation and Verification, Completed 8/4/16

C SP 600.13, P-82 Electric Fire Pump Annual Operability Demonstration, Completed 5/19/16 &

9/17/16

C SP 600.14, P-82 Electric Fire Pump Annual Operability Demonstration, Completed 12/4/14 &

12/4/15

C SP 600.16 Fire Protection System Underground Main Flush & Flow Test, Completed 10/13/10

& 10/9/13

C SP 600.18, Unit 2 Fire Hose Station Inspection, Completed 6/22/16

C SP 600.22, Unit 2 Fire Hose Station Flow Test, Completed 2/13/15

C SP 600.24, Unit 2 Fire Brigade Equipment Inspection, Completed 4/24/16

C SP 600.24, Unit 2 Fire Brigade Equipment Inspection, Completed 5/25/16

C SP 600.25, Unit 2 Fire Door Inspection, Completed 6/20/16

C SP 600.25, Unit 3 Fire Door Inspection, Completed 9/3/15

C SP 600.28, Fire Brigade Vehicle Equipment Inspection Data Sheet (R1), Completed 5/21/16

C SP 600.6, Electric Fire Pump M7-8 Monthly Operability Demonstration, Completed 5/10/16 &

6/3/16

C SP 600.7, Electric Fire Pump M7-8 Annual Operability Demonstration, Completed 12/22/14 &

12/19/15

C SP 600.8, Diesel Fire Pump M7-7 Monthly Operability Demonstration, Completed 5/13/16 &

6/8/16

C SP 600.9, Diesel Fire Pump M7-7 Annual Operability Demonstration, Completed 8/6/15 &

6/8/16

C SP 788A, Fire Pump Diesel Engine Battery Quarterly Surveillance, Completed 6/16/16

C SP 788B, Fire Pump Diesel Engine Battery 18-Month Surveillance, Completed 6/10/16

C SP 788C, Fire Pump Diesel Engine Battery Weekly Surveillance, Completed 6/16/16

CSP 600.24, Fire Brigade Equipment Inspection, Completed 6/3/16

SFP 17, Unit 3 Fire Penetration Seal and Barrier Inspection- Group 1, Completed 2/10/06

SFP 17, Unit 3 Fire Penetration Seal and Barrier Inspection- Group 4, Completed 2/9/11

SFP 17, Unit 3 Fire Penetration Seal and Barrier Inspection- Group 4, Completed 10/9/14

SFP 17, Unit 3 Fire Penetration Seal and Barrier Inspection- Group 9, Completed 12/27/13

SFP 21, Unit 2 Appendix R Fire Cage Inventory, Completed 11/25/15

SFP 9, Unit 3 - Fire Extinguisher Inspection Data Sheet - Train B, Completed 6/29/16

SFP 9, Unit 3 - Fire Extinguisher Inspection Data Sheet - Train A, Completed 7/11/16

SFP Procedure 21, Unit 3 Safe Shutdown Fire Cage Inventory, Completed on 11/26/2015

SP 2402CR, Steam Generator Pressure Rack Instrument Calibration, Revision 0, Completed

8/12/14 and 3/16/16

SP 2601P, Unit 2 CVCS Valve Operability Tests from C-10 and C-02, Revision 0, Completed

10/30/15

SP 2610B, Turbine Driven Auxiliary Feed Pump Operational Tests from C-10, Completed 3/2/16

SP 2610E, Atmospheric Dump Valve Testing From C-10, C-70A and C-70B, Completed

10/21/15

SP 2610M, Power Operated Relief Valve Hot Functional Test, Completed 11/1/15

SP 2657, EOP Equipment Inventory, Completed 9/7/15

SP 3442J01, RCS Wide Range Pressure Rack Calibration, Completed 9/16/14 and 2/11/16

SP 3444A02, Steam Generator Water Level Wide Range Calibration, Completed 7/10/13 and

3/11/15

A-7

SP 3451Q01, Unit 3 Instrument Rack Room and Fire Pump House - Halon Fire System Test,

Completed 2/26/16

SP 3641B.2, IRR Halon System Flow Test, Completed 5/17/15

SP 3641B.2, IRR Halon System Flow Test, Completed 5/8/14

SP 3641D.3, Fire Protection Zone Panel 3B Detector Operability Checks, Completed 1/8/15

SP 3641D.3, Fire Protection Zone Panel 3B Detector Operability Checks, Completed 1/19/13

SP 3641D.3, Fire Protection Zone Panel 3B Detector Operability Checks, Completed 12/21/14

SP 3641D.3, Fire Protection Zone Panel 5C EDG A Area Detector Operability Checks,

Completed 2/25/16

SP 3641D.5, Fire Damper Operability Verification, Completed 1/25/06

SP 3641D.5, Fire Damper Operability Verification, Completed 5/8/11

SP 3641D.5, Fire Damper Operability Verification, Completed 9/5/99

SP 3641D.6, Fire Rated Assemblies Inspection, Completed 8/2/15

SP 3641F.1, Functional Check of the East and West Switchgear Breathing Air System,

Completed 6/21/15

SP 3672.2-10, Fire Transfer Switch Panel Operational Testing-3RCS*PCV455A, Completed

11/9/14

SP 3672.2-2, Fire Transfer Switch Panel Operational Testing-3HVP*FN1A and FN1C,

Completed 3/20/12

SP 3672.2-7, Fire Transfer Switch Panel Operational Testing-3SWP*MOV54A and MOV54C,

Completed 8/1/13

SP 3672.2-8, Fire Transfer Switch Panel Operational Testing-3SWP*MOV71A Completed

11/23/15

SP 3673.2, Unit 3 Fire Transfer Switch Panel Operational Testing for 3HVP*FN1A and

3HVP*FN1C, Completed 3/20/12

SP 3673.2, Unit 3 Fire Transfer Switch Panel Operational Testing for 3HVR*FN14A, Completed

10/25/14

SP 3673.2, Unit 3 Fire Transfer Switch Panel Operational Testing for 3HVR*MOD50A,

Completed 12/20/12

SP 3673.2, Unit 3 Fire Transfer Switch Panel Operational Testing for 3HVR*ACU1A, Completed

12/22/15

SP 3673.2, Unit 3 Fire Transfer Switch Panel Operational Testing for 3HVY*FN2A, Completed

12/18/12

SP 3673.2, Unit 3 Fire Transfer Switch Panel Operational Testing for 3SWP*MOV71A,

Completed 11/23/15

SP 3673.4, Auxiliary Shutdown Panel Operability Test for Charging Injection Path, Completed

5/1/16

SP 3673.4, Auxiliary Shutdown Panel Operability Test for Charging Isolation Path, Completed

5/1/16

SP 3673.4, Auxiliary Shutdown Panel Operability Test for Train A CVCS Components,

Completed 1/14/15

SP 3673.4-001, Auxiliary Shutdown Panel Operability Test, Completed 5/8/16

SP 3673.4-004, Auxiliary Shutdown Panel Operability Test Train A Auxiliary Feedwater

Components, Completed 2/8/15

SP 3673.4-007, Auxiliary Shutdown Panel Operability Test Train B Auxiliary Feedwater

Components, Completed 2/1/15

SP 3673.4-009, Auxiliary Shutdown Panel Operability Test Train B CVCS Components,

Completed 5/22/16

A-8

SP 3673.4-011, Auxiliary Shutdown Panel Operability Test Train A PORV and Block Valves,

Completed 1/9/14

SP 3673.4-014, Auxiliary Shutdown Panel Operability Test Non-Train Related Components,

Completed 5/1/16

SP2618C, Smoke and Heat Detector Testing, Auxiliary Building, Completed 3/24/16

SP2618C, Smoke Detector Testing, Switchgear Detector Testing, Facility 1, Completed 5/30/16

SP2618C, Smoke Detector Testing, Turbine Building, Completed 1/19/16

SP2618C, Turbine Bldg. 256 Cable Vault and Vertical Shaft Smoke Detector Test, Completed

3/4/16

SP2618D, A DG Deluge Systems Design Function Test, Completed 1/12/16

SP2618D, Fire Protection System sprinkler and Deluge Design Function test, Completed

5/20/15

SP2618H, Fire Protection System Deluge Nozzle Flow Test, Completed 7/16/14

SP2618L, Fire Protection Coating Inspection, Completed 8/4/15

SP2618L, TSI Fire Wrap Inspection, Completed 8/7/15

SP2657, Inventory Remote Shutdown Station Storage, Completed 5/13/16

Operating Experience Evaluations

Information Notice 2014-10, Potential Circuit Failure-Induced Secondary Fires or Equipment

Damage, dated 9/16/14

Quality Assurance Audits and Self Assessments

Audit 15-04, Fire Protection Program, dated 7/15/15

System Health Reports

3341 A, B, C, F - Fire Protections Water, Halon, CO2, Emerg. Breathing Air, dated

10/1/14- 12/31/14

3341 A, B, C, F - Fire Protections Water, Halon, CO2, Emerg. Breathing Air, dated

10/1/15- 12/31/15

3341D - Fire Detection, dated 10/1/14- 12/31/14

3341D - Fire Detection, dated 10/1/15- 12/31/15

ELU System Health Report, 1St Quarter 2016

ELU System Health Report, 4th Quarter 2015

Program/Comp Health Report FP- Fire Protection - Including Appendix R, 4th Quarter 2015

Program/Comp Health Report FP- Fire Protection - Including Appendix R, 1st Quarter 2016

System Health Report 2352, 3720B - Safe Shutdown Lighting, 1st Quarter 2016

System Health Report 2352, 3720B - Safe Shutdown Lighting, 4th Quarter 2015

U 2 Fire Protection & Deluge, CO2 Alterex, Halon Supression, 4th Quarter 2014

U 2 Fire Protection & Deluge, CO2 Alterex, Halon Supression, 4th Quarter 2015

Unit 2 AC and DC Systems, 4th qtr. 2015 and 1st Quarter 2016

Unit 3 AC and DC Systems, 4th qtr. 2015 and 1st Quarter 2016

A-9

Drawings and Wiring Diagrams

12179-30276, U3 Generator Seal Oil System Emergency Seal Oil pump 3GMO-P2 Control,

Revision 5

12179-FIG-77B, Fire Hazard Analysis Plan Elevation 24 Feet 6 inch, Revision 6

12179-FIG-77C, Fire Hazard Analysis Plant Elevation 38 Feet 6 inch, Revision 11

25203-24070, Sheet 10, RCP Oil Collection System Details for RCP Motor in Cubicle A,

Revision 2

25203-24070, Sheet 11, RCP Oil Collection System Details for RCP Motor in Cubicle A,

dated 5/16/95

25203-24070, Sheet 12, RCP Oil Collection System Details for RCP Motor in Cubicle A,

dated 4/19/95

25203-24070, Sheet 13, RCP Oil Collection System Details for RCP Motor in Cubicle A,

dated 4/20/95

25203-28500, Sht.356, Unit 2 PT-1023B Steam Generator Pressure Loop Diagram, Revision 10

25203-30001, Unit 2 Main Single Line Diagram, Revision 40

25203-30005, Unit 2 Single Line Meter and Relay Diagram 4.16kV Emergency Buses 24C and

24D, Revision 21

25203-30009, Unit 2 Single Line Meter and Relay Diagram 4.16kV Emergency Buses 25E and

24G, Revision 13

25203-30022, Sht. 3, Unit 2 DV20 125Vdc and 120Vac Distribution Panel Schedule, Revision

21

25203-30023, U2 Single Line Diagram 125VDC System-Turbine Battery, Revision 9

25203-30024, U2 Single Line Diagram 125VDC Emergency & 120VAC Vital Systems, Revision

39

25203-30053, Sheet 1, U2 Schematic Diagram 125VDC Switchgear Bus D01, Revision 7

25203-30053, Sheet 3, U2 Schematic Diagram 125VDC Switchgear Bus D02, Revision 9

25203-30053, Sheet 5, U2 Switchgear Diagram 125VDC Switchgear Bus D03, Revision 10

25203-30102, Unit 2 Instrument Rack Loading Diagram Fire Shutdown Panel C09, Revision 3

25203-32002, Sh. 16, 4.16kV Switchgear Kirk Key Interlocks, Revision 5

25203-32006, Sheet 13, U2 Magnetic Starter Elementary Diagram, Revision 8

25203-32009, Sht. 37, Unit 2 Charging Line Distribution Solenoid Valve CH519, Revision 9

25203-32009, Sht. 41, Unit 2 Charging Pump Control MP18B, Revision 23

25203-32009, Sht. 42A, Unit 2 Charging Pump Control MP18B, Revision 3

25203-32009, Sht. 6, Unit 2 Volume Control Tank Discharge MOV CH501, Revision 13

25203-34051, Unit 2 Auxiliary Building Miscellaneous Plan Section and Details, Revision 40

25203-39076, Sheet 9A, U2 Magnetic Starter Elementary Diagram, Revision 1

25203-39076, Sheet 9B, U2 Magnetic Starter Elementary Diagram, Revision 1

25203-39220, Sht. 1B, Unit 2 Instrument Rack Loading Diagram Spec 200 Cabinet RC30B,

Revision 19

25203-39352, Sheet 1, U2 One Line Diagram, 15KVA Inverter VIP1 & Static Sw. VS1,

Revision 5

25203-39353, Sheet 1, U2 One Line Diagram, 15KVA Inverter VIP2 & Static Sw. VS2,

Revision 5

25203-39354, Sheet 1, U2 One Line Diagram, 15KVA Inverter VIP3 & Static Sw. VS3,

Revision 5

25203-39355, Sheet 1, U2 One Line Diagram, 15KVA Inverter VIP4 & Static Sw. VS4,

Revision 3

25203-39356, Sheet 1, U2 One Line Diagram, 15KVA Inverter VIP5, Revision 5

A-10

25203-39357, Sheet 1, U2 One Line Diagram, 15KVA Inverter VIP6, Revision 6

25203-39367, Sheet 6, U2 Schematic Totalizing Box Turbine Battery Charger 201D/DC4,

Revision 2

25205-25003, Station Fire Loop Operating & Hydraulic Analysis Schematic, Revision 14

25212-24036, Fire Stop & Seals Map Locations, Revision 0

25212-24037, Fire Stop & Seals Map Locations, Revision 0

25212-24273, Wall Pene. Map Aux. BLDG. EL. 45-6, Revision 2

25212-29367 SH 20, Fire Protection & Detection Systems, dated 6/2/75

25212-29680 SH.0010, TCO-003 High Density Silicone Elastomer Fire, Air, and/or Radiation

Seal for Electrical Blockout Openings, dated 8/20/84

25212-29680 SH.0023, TCO-050 Silicone Foam Fire or Air Seals for Sleeve, Conduit, Cast or

Core Bored Openings up to 5 Dial, dated 1/26/85

25212-30001, Unit 3 Main One Line Diagram, Revision 26

25212-30004, Unit 3 Main One Line Diagram 4160V Normal and Emergency Buses, Revision

20

25212-30010, Unit 3 6900V One Line Diagram Bus 35A and 35B, Revision 20

25212-30011, Unit 3 6900V One Line Diagram Bus 35C and 35D, Revision 21

25212-30027, Sht. 3, Unit 3 480V Motor Control Center One Line Diagram Auxiliary Building,

Revision 44

25212-30272, Sht. 29A, Unit 3 Feedwater System Steam Generator 3RCS*SG1A Wide Range

Level Indication, Revision 8

25212-30272, Sht. 30, Feedwater System Steam Generator 3RCS*SG1A, Revision 5

25212-30343, Sht. 10A, Unit 3 Reactor Coolant System Channel 1 Wide Range Pressure Loop

Diagram, Revision 6

25212-30343, Sht. 10B, Unit 3 Reactor Coolant System Channel 1 Wide Range Pressure Loop

Diagram, Revision 5

25212-30343, Sht. 10C, Unit 3 Reactor Coolant System Channel 1 Wide Range Pressure Loop

Diagram, Revision 5

25212-30343, Sht. 11, Unit 3 Reactor Coolant System Channel 1 Wide Range Pressure Loop

Diagram, Revision 5

25212-30379, Sheet 8, U3 Turbine Generator Lube Oil System Emergency Bearing Oil Pump

Control, Revision 3

25212-3200, Sht. 7, Elementary Diagram Reactor Head Vent Isolation Valves

3RCS*SV8095A(B), Revision 6

25212-32001, Elementary Diagram 480V MCC Charging Header Isolation Valve

2CHS*MV8438A, Revision 15

25212-32001, Sheet 6CI, U3 Elementary Diagram 125VDC Emergency Bearing Oil Pump

[3TML-P1], Revision 10

25212-32001, Sheet 6CS, U3 Elementary Diagram 125VDC Generator Emergency Seal Oil

Pump [3GMO-P2], Revision 14

25212-32001, Sht. 7DX, Elementary Diagram Letdown Line Isolation Valves 3RCS*LCV459 and

3RCS*LCV460, Revision 9

25212-32068, U3 Elementary Diagram Diesel Driven Fire Pump M7-7 Control Circuit, Revision

2

25212-39002, Sheet 1020, U3 DC Starter Emergency Seal Oil Elementary, Revision D

25212-39002, Sheet 1021, U3 DC Starter Emergency Seal Oil Schematic, Revision C

25212-39002, Sheet 1062, U3 Emergency Bearing Oil Pump Starter-Outline Schematic & Conn.

Diagram, Revision E

A-11

SKE-3.1-ELEC DIST, Emergency System One Line Diagram for Appendix R, Revision 2

Piping and Instrumentation Diagrams

25203-26005, Sht. 2, Unit 2 P&ID Feed System, Revision 73

25203-26008, Sh. 2, Piping and Instrumentation Diagram Service Water, Revision 114

25203-26011, Fire Protection, Revision 57

25203-26014, Sht. 1, Unit 2 P&ID Reactor Coolant System, Revision 41

25203-26014, Sht. 2, Unit 2 P&ID Reactor Coolant System, Revision 46

25203-26017, Sht. 1, Unit 2 P&ID Charging System, Revision 63

25212-25008, Yard Water & Fire Protection Piping, Revision 29

25212-25009, Yard Water & Fire Protection Piping, Revision 24

25212-26902, Sht. 1, Unit 3 P&ID Reactor Coolant System, Revision 33

25212-26902, Sht. 3, Unit 3 P&ID Reactor Coolant System, Revision 25

25212-26904, Sht. 1, Unit 3 P&ID Chemical and Volume Control, Revision 54

25212-26904, Sht. 2, Unit 3 P&ID Chemical and Volume Control, Revision 17

25212-26905, Sht. 1, Unit 3 P&ID Charging Pump Seal and Lubrication, Revision 33

25212-26921, Sht. 1, Unit 3 P&ID Component Cooling Water, Revision 33

25212-26970, Fire Protection System, Revision 12

Pre-Fire Plans

Fire Area AB-6, Auxiliary Building West MCC and Rod Control Area, Revision 0

Fire Area CB-11, Control Building Instrument Rack Room Underfloor Area, Revision 0

Fire Area EG-3, Emergency Generator North Emergency generator Enclosure, Revision 0

Fire Area ESF-3, Engineered Safety Features Building North Residual Heat Removal Heat

Exchanger Cubicle, Revision 0

MP2 Fire Fighting Strategies, Unit 2, Fire Area A-15, Diesel Generator A Cubicle, Revision 0

MP2 Fire Fighting Strategies, Unit 2, Fire Area A-32, Air Handling Units 386, Revision 0

MP2 Fire Fighting Strategies, Unit 2, Fire Area T-7, 69. And 4.16 KV Switchgear Room,

Revision 0

MP2 Fire Fighting Strategies, Unit 2, Fire Area T-9, East 45 Cable Vault (Z1 train), Revision 0

Fire Drills and Critiques

Fire in Building 454, Completed 6/7/16

Fire in U1 Maintenance Shop, Completed 12/14/15

Fire in U2 H2 Seal Oil Skid Pass, Completed 6/18/15

Fire in U2 Intake, Completed 12/4/15

Fire in U2 Lube Oil Room, Completed 6/9/15

Fire in U2 Upper 4160 Switch Gear, Completed 4/28/15

Fire in U3 Maintenance Shop, Completed 12/12/15

Fire Brigade Training

B5b Familiarization PowerPoint Presentation

B5b Hands-On Training attendance records, dated 5/12/15 and 11/17/15

Beyond Design Basis, Non-Licensed Operator Training Presentation

A-12

Operator Safe Shutdown Training

15605L, EOP 3509.1 Self-Guided in Plant Walkdown, Revision 0

AOP 2559 - Fire AOP 2579A/AA - Appendix R Fire in R-1, Aux Bldg including Control

Room/Computer Rooms/25 Cable Vault, Millstone Unit 2 Licensed Operator Training

Program Slides

ASP115C, Auxiliary Shutdown Equipment/Auxiliary Shutdown Panel Lesson Plan, Revision 3

C15506N, MP3*NLCT*EOP 3509.1, Revision 0

Common Operating Procedure 200.18 Time Critical Action Validation and Verification Slides,

dated 7/12/16

JPM P003, Isolate Emergency Bus 34C in Accordance with EOP 3509.1, Revision 7

JPM P011 (MC-00094), Primary Side Plant Equipment Operator (PEO) Actions on a Control

Room Evacuation (Parts 1 and 2), Revision 9/0

JPM P012, Secondary Side PEO Actions on a Control Room Evacuation, Revision 6

JPM P015, Secondary Side PEO Actions on a Control Room Evacuation due to Fire, Revision 8

JPM P173, Aligning the Fire Transfer Switch Panel and Auxiliary Shutdown Panel in Response

to a Fire, Revision 2

JPM P188, Installation of 3CHS-PI102T, Revision 0

JPM P209, Cross-Connect Service Water to East Switchgear Ventilation, Revision 1

SEG S13406L, Respond to a Control Room, Cable Spreading Area or Instrument Rack Room

Fire, Revision 0

SEG S15304L, Fire in Instrument Rack Room, Revision 0

Unit 2 Licensed Operator Requalification Program Attendance Sheet for Cycle 16-3, 5/10 - 6/17

Hot Work and Ignition Source Permits, and Transient Combustible Permits and Evaluations

29633-12-FP

30391-13-IS

31960-15-IS

41224-12-FP

41316-12-FP

41399-12-IS

43879-15-FP

43965-15-IS

44356-16-FP

44385-16-IS

44389-16-IS

44390-16-IS

44499-16-FP

Corrective Action Program Documents (Condition Reports)

463259

515160

520964

522469

522722

522740

522848

522850

523785

527755

530987

541980

541983

553343

557088

576367

578178

578333

581890

582625

582652

582665

1004974

1009069

1037462

1041883

1042283*

1043063*

1043417*

1043422*

1043425*

1043455*

1043458*

1043959*

1044278*

1044301*

1044326*

1044332*

1044334*

1044348*

1044422*

1044536*

1044760*

  • NRC identified during this inspection.

A-13

Work Orders

53M20807693

53012768647

53102490410

53102502011

53102582983

53102605405

53102649190

53102656386

53102659739

53102669361

53102693811

53102695870

53102698825

53102698915

53102698922

53102698928

53102698931

53102716240

53102716256

53102732991

53102735138

53102759052

53102760642

53102764120

53102786767

53102814722

53102846681

53102853315

53102854686

53102861679

53102871440

53102873143

53102887195

53102892290

53102900241

53102905692

53102914238

53102952946

53102958935

Vendor Manuals

25212-902-001, Vendor Technical Manual for Emergency Lighting from Exide, Holophane,

Dualite, Birns, Revision 6

TI 2AI-130, Spec 200 Current-To-Voltage Converters, dated 10/77

Industry Standards

NFPA 10-1968, Installation for Portable Fire Extinguishers

NFPA 13-1971, Installation of Sprinkler Systems

NFPA 14-1978, Installation of Standpipe and Hose Systems

NFPA 15-1985, Water Spray for Fixed Systems for Fire Protection

NFPA 27-1975, Private Fire Brigade

NFPA 72D-1986, Maintenance and Use of Proprietary protective Signaling Systems

NFPA 72E-1984, Automatic Fire Detectors

Miscellaneous Documents

Aid Agreement letter Between Millstone and the Waterford Fire Service, dated 8/6/15

Electrical Cable and Conduit Routing Information - SAFE

Fire and Hose-Stream tests for Penetration Seal Systems, dated 4/82

Fire Qualification Test on Floor Penetration Seals, dated 11/30/79

Hazard Evaluation Sheet Building - CB, dated 12/11/85

Millstone Site Fire Protection Active Impairment List, dated 7/11/16

Millstone Site Fire Protection Active Impairment List, dated 7/26/16

Millstone Site Fire Protection Active Impairment List, dated 7/27/16

Waterford Ambulance Service Memorandum of Understanding (MOU), dated 8/5/15

Waterford Fire Service MOU, dated 8/6/15

Waterford Police Department MOU, dated 9/14/15

A-14

LIST OF ACRONYMS

ADAMS

Agencywide Documents Access and Management System

ADV

Atmospheric Dump Valve

AFW

Auxiliary Feedwater

AOP

Abnormal Operating Procedure

BTP

Branch Technical Position

CAP

Corrective Action Program

CFR

Code of Federal Regulations

CMEB

Chemical Engineering Branch

CO2

Carbon Dioxide

CONVEX

Connecticut Valley Electric Exchange

CR

Condition Report

CSD

Cold Shutdown

DC

Direct Current

Dominion

Dominion Nuclear Connecticut, Inc.

DRS

Division of Reactor Safety

EDG

Emergency Diesel Generator

EOP

Emergency Operating Procedure

FA

Fire Area

FHA

Fire Hazards Analysis

FPP

Fire Protection Program

FSAR

Final Safety Analysis Report

FZ

Fire Zone

IEEE

Institute of Electrical and Electronics Engineering

IMC

Inspection Manual Chapter

IP

Inspection Procedure

IPEEE

Individual Plant Examination of External Events

IR

Inspection Report

LER

Licensee Event Report

LOOP

Loss of Offsite Power

Millstone

Millstone Power Station Unit 2 and Unit 3

NCV

Non-Cited Violation

NFPA

National Fire Protection Association

NRC

Nuclear Regulatory Commission

OMA

Operator Manual Action

P&ID

Piping and Instrumentation Drawing

PARS

Publicly Available Records System

RAS

Reasonable Assurance of Safety

SBO

Station Blackout

SDP

Significance Determination Process

SER

Safety Evaluation Report

SFP

Site Fire Protection

SG

Steam Generator

UFSAR

Updated Final Safety Analysis Report

V

Volts

V dc

Voltage Direct Current