IR 05000324/2017002: Difference between revisions

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| number = ML17212A137
| number = ML17212A137
| issue date = 07/31/2017
| issue date = 07/31/2017
| title = Brunswick Steam Electric Plant - NRC Integrated Inspection Report Nos. 05000325/2017002 and 05000324/2017002 and Exercise of Enforcement Discretion
| title = NRC Integrated Inspection Report Nos. 05000325/2017002 and 05000324/2017002 and Exercise of Enforcement Discretion
| author name = Rose S D
| author name = Rose S
| author affiliation = NRC/RGN-II/DRP/RPB4
| author affiliation = NRC/RGN-II/DRP/RPB4
| addressee name = Gideon W R
| addressee name = Gideon W
| addressee affiliation = Duke Energy Progress, Inc
| addressee affiliation = Duke Energy Progress, Inc
| docket = 05000324, 05000325
| docket = 05000324, 05000325
Line 19: Line 19:


=Text=
=Text=
{{#Wiki_filter:
{{#Wiki_filter:July 31, 2017
[[Issue date::July 31, 2017]]


EA-17-123 William Site Vice President Brunswick Steam Electric Plant 8470 River Rd. SE (M/C BNP001) Southport, NC 28461
==SUBJECT:==
 
BRUNSWICK STEAM ELECTRIC PLANT - NRC INTEGRATED INSPECTION REPORT NOS.: 05000325/2017002 AND 05000324/2017002 AND EXERCISE OF ENFORCEMENT DISCRETION
SUBJECT: BRUNSWICK STEAM ELECTRIC PLANT - NRC INTEGRATED INSPECTION REPORT NOS.: 05000325/2017002 AND 05000324/2017002 AND EXERCISE OF ENFORCEMENT DISCRETION


==Dear Mr. Gideon:==
==Dear Mr. Gideon:==
On June 30, 2017, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Brunswick Steam Electric Plant, Units 1 and 2. On July 12, 2017, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.
On June 30, 2017, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Brunswick Steam Electric Plant, Units 1 and 2. On July 12, 2017, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.


A violation of Technical Specification 3.6.4.1, Secondary Containment, was identified. Because the violation was identified during the discretion period described in Enforcement Guidance Memorandum 11-003, Revision 3, the NRC is exercising enforcement discretion in accordance with Section 3.5, "Violations Involving Special Circumstances," of the NRC Enforcement Policy and, therefore, will not issue enforcement action for this violation, subject to the license amendment request which was submitted on June 29, 2017. Further, inspectors documented a licensee-identified violation which was determined to be of very low safety significance in this report. The NRC is treating this violation as non-cited violation (NCV) consistent with Section 2.3.2.a of the Enforcement Policy.
A violation of Technical Specification 3.6.4.1, Secondary Containment, was identified. Because the violation was identified during the discretion period described in Enforcement Guidance Memorandum 11-003, Revision 3, the NRC is exercising enforcement discretion in accordance with Section 3.5, Violations Involving Special Circumstances, of the NRC Enforcement Policy and, therefore, will not issue enforcement action for this violation, subject to the license amendment request which was submitted on June 29, 2017.
 
Further, inspectors documented a licensee-identified violation which was determined to be of very low safety significance in this report. The NRC is treating this violation as non-cited violation (NCV) consistent with Section 2.3.2.a of the Enforcement Policy.
 
If you contest the violation or the significance of the violation, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator Region II; the Director, Office of Enforcement, and the NRC Resident Inspector at the Brunswick Steam Electric Plant. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.
 
Sincerely,
/RA/


If you contest the violation or the significance of the violation, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator Region II; the Director, Office of Enforcement, and the NRC Resident Inspector at the Brunswick Steam Electric Plant. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, "Public Inspections, Exemptions, Requests for Withholding."
Steven D. Rose, Chief Reactor Projects Branch 4 Division of Reactor Projects


Sincerely,/RA/ Steven D. Rose, Chief Reactor Projects Branch 4 Division of Reactor Projects Docket Nos.: 50-325, 50-324 License Nos.: DPR-71, DPR-62  
Docket Nos.: 50-325, 50-324 License Nos.: DPR-71, DPR-62  


===Enclosure:===
===Enclosure:===
IR 05000325, 324/2017002  
IR 05000325, 324/2017002 w/Attachment: Supplementary Information
 
REGION II==
Docket Nos.:
50-325, 50-324
 
License Nos.:
DPR-71, DPR-62
 
Report No.:
05000325/2017002, 05000324/2017002  


===w/Attachment:===
Licensee:
Supplementary Information
Duke Energy Progress, Inc.


cc Distribution via ListServ
Facility:
Brunswick Steam Electric Plant, Units 1 & 2


ML17212A137 OFFICE RII:DRP RII:DRP RII: DRP RII:DRP RII:DRP RII:EICS NAME MSchwieg MCatts DJackson JDodson SRose MKowal DATE 7/19/2017 7/24/2017 7/19/2017 7/27/2017 7/28/2017 7/26/2017 Enclosure U.S. NUCLEAR REGULATORY COMMISSION REGION II Docket Nos.: 50-325, 50-324
Location:
Southport, NC


License Nos.: DPR-71, DPR-62
Dates:
April 1, 2017 through June 30, 2017


Report No.: 05000325/2017002, 05000324/2017002 Licensee: Duke Energy Progress, Inc.
Inspectors:  


Facility: Brunswick Steam Electric Plant, Units 1 & 2 Location: Southport, NC
M. Catts, Senior Resident Inspector M. Schwieg, Resident Inspector D. Jackson, RII Project Engineer


Dates: April 1, 2017 through June 30, 2017 Inspectors: M. Catts, Senior Resident Inspector M. Schwieg, Resident Inspector D. Jackson, RII Project Engineer
Approved by:
Steven D. Rose, Chief Reactor Projects Branch 4


Approved by: Steven D. Rose, Chief Reactor Projects Branch 4 Division of Reactor Projects  
Division of Reactor Projects  


=SUMMARY=
=SUMMARY=
Integrated Inspection Report 05000325/2017002, 05000324/2017002; April 1, 2017, through June 30, 2017; Brunswick Steam Electric Plant, Units 1 and 2.
Integrated Inspection Report 05000325/2017002, 05000324/2017002; April 1, 2017, through  
 
June 30, 2017; Brunswick Steam Electric Plant, Units 1 and 2.


The report covered a 3-month period of inspection by resident inspectors and regional inspectors. There were no NRC-identified or self-revealing violations documented in this report.
The report covered a 3-month period of inspection by resident inspectors and regional inspectors. There were no NRC-identified or self-revealing violations documented in this report.


The significance of inspection findings are indicated by their color (i.e., greater than Green, or Green, White, Yellow, Red) and determined using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process," (SDP) dated April 29, 2015. All violations of NRC requirements are dispositioned in accordance with the NRC's Enforcement Policy dated November 1, 2016. The NRC's program for overseeing the safe operations of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 6. One violation of very low safety significance that was identified by the licensee has been reviewed by the NRC. Corrective action taken or planned by the licensee has been entered into the licensee's corrective action program (CAP). This violation and corrective action tracking number is listed in Section 4OA7 of this report.
The significance of inspection findings are indicated by their color (i.e., greater than Green, or Green, White, Yellow, Red) and determined using Inspection Manual Chapter (IMC) 0609,
Significance Determination Process, (SDP) dated April 29, 2015. All violations of NRC requirements are dispositioned in accordance with the NRCs Enforcement Policy dated November 1, 2016. The NRCs program for overseeing the safe operations of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 6.
 
One violation of very low safety significance that was identified by the licensee has been reviewed by the NRC. Corrective action taken or planned by the licensee has been entered into the licensees corrective action program (CAP). This violation and corrective action tracking number is listed in Section 4OA7 of this report.


=REPORT DETAILS=
=REPORT DETAILS=


===Summary of Plant Status===
===Summary of Plant Status===
Unit 1 began the inspection period at 100 percent rated thermal power (RTP). On April 25, 2017, the unit was shut down for a forced outage to repair the 1B recirculation pump seal. On April 28, 2017, the unit was restarted and power was returned to 100 percent on May 1, 2017. On May 2, 2017, power was reduced to 66 percent for a control rod improvement and power was returned to 100 percent on May 4, 2017. On May 6, 2017, power was reduced to 80 percent for a control rod improvement and power was returned to 100 percent on May 8, 2017. On May 31, 2017, power was reduced to 98 percent due to a loss of the 1B variable frequency device controller for the 1B recirculation pump. Power was returned to 100 percent after restoration of the 1B variable frequency device controller on May 31, 2017. On June 9, 2017, power was reduced to 70 percent for a control rod improvement and power was returned to 100 percent on June 11, 2017. The unit remained at or near 100 percent RTP for the remainder of the inspection period.
Unit 1 began the inspection period at 100 percent rated thermal power (RTP). On April 25, 2017, the unit was shut down for a forced outage to repair the 1B recirculation pump seal. On April 28, 2017, the unit was restarted and power was returned to 100 percent on May 1, 2017. On May 2, 2017, power was reduced to 66 percent for a control rod improvement and power was returned to 100 percent on May 4, 2017. On May 6, 2017, power was reduced to 80 percent for a control rod improvement and power was returned to 100 percent on May 8, 2017. On May 31, 2017, power was reduced to 98 percent due to a loss of the 1B variable frequency device controller for the 1B recirculation pump. Power was returned to 100 percent after restoration of the 1B variable frequency device controller on May 31, 2017.
 
On June 9, 2017, power was reduced to 70 percent for a control rod improvement and power was returned to 100 percent on June 11, 2017. The unit remained at or near 100 percent RTP for the remainder of the inspection period.


Unit 2 began the inspection period shutdown for refueling outage B223R1. On April 14, 2017, the unit was restarted and power was returned to 100 percent on April 22, 2017. On May 22, 2017, power was reduced to 70 percent to repair a steam leak on 2-MD-V16 and power was returned to 100 percent on May 22, 2017. On June 3, 2017, power was reduced to 70 percent for a control rod sequence exchange and valve testing. Power was returned to 100 percent on June 3, 2017. On June 5, 2017, power was reduced to 70 percent for a control rod sequence exchange. Power was returned to 100 percent on June 5, 2017. The unit remained at or near 100 percent RTP for the remainder of the inspection period.
Unit 2 began the inspection period shutdown for refueling outage B223R1. On April 14, 2017, the unit was restarted and power was returned to 100 percent on April 22, 2017. On May 22, 2017, power was reduced to 70 percent to repair a steam leak on 2-MD-V16 and power was returned to 100 percent on May 22, 2017. On June 3, 2017, power was reduced to 70 percent for a control rod sequence exchange and valve testing. Power was returned to 100 percent on June 3, 2017. On June 5, 2017, power was reduced to 70 percent for a control rod sequence exchange. Power was returned to 100 percent on June 5, 2017. The unit remained at or near 100 percent RTP for the remainder of the inspection period.


==REACTOR SAFETY==
==REACTOR SAFETY==
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity  
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity  
{{a|1R01}}
 
{{a|1R01}}
 
==1R01 Adverse Weather Protection==
==1R01 Adverse Weather Protection==
{{IP sample|IP=IP 71111.01|count=1}}
{{IP sample|IP=IP 71111.01|count=1}}


====a. Inspection Scope====
====a. Inspection Scope====
Seasonal Extreme Weather Conditions The inspectors conducted a detailed review of the station's adverse weather procedures written for extreme high temperatures. The inspectors verified that weather-related equipment deficiencies identified during the previous year had been placed into the work control process and/or corrected before the onset of seasonal extremes. The inspectors evaluated the licensee's implementation of adverse weather preparation procedures and compensatory measures before the onset of seasonal extreme weather conditions. Documents reviewed are listed in the Attachment.
Seasonal Extreme Weather Conditions  
 
The inspectors conducted a detailed review of the stations adverse weather procedures written for extreme high temperatures. The inspectors verified that weather-related equipment deficiencies identified during the previous year had been placed into the work control process and/or corrected before the onset of seasonal extremes. The inspectors evaluated the licensees implementation of adverse weather preparation procedures and compensatory measures before the onset of seasonal extreme weather conditions.
 
Documents reviewed are listed in the Attachment.


The inspectors evaluated the following risk-significant systems:
The inspectors evaluated the following risk-significant systems:
Line 83: Line 115:


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R04}}
{{a|1R04}}
 
==1R04 Equipment Alignment==
==1R04 Equipment Alignment


====a. Inspection Scope====
====a. Inspection Scope====
Partial Walkdown (71111.04 - 4 samples) The inspectors verified that critical portions of the selected systems were correctly aligned by performing partial walkdowns. The inspectors selected systems for assessment because they were a redundant or backup system or train, were important for mitigating risk for the current plant conditions, had been recently realigned, or were a single-train system. The inspectors determined the correct system lineup by reviewing plant procedures and drawings. Documents reviewed are listed in the Attachment. The inspectors selected the following systems or trains to inspect:
Partial Walkdown (71111.04 - 4 samples)  
 
==
The inspectors verified that critical portions of the selected systems were correctly aligned by performing partial walkdowns. The inspectors selected systems for assessment because they were a redundant or backup system or train, were important for mitigating risk for the current plant conditions, had been recently realigned, or were a single-train system. The inspectors determined the correct system lineup by reviewing plant procedures and drawings. Documents reviewed are listed in the Attachment.
 
The inspectors selected the following systems or trains to inspect:
* Unit 1, core spray (CS) train B
* Unit 1, core spray (CS) train B
* Unit 2, reactor core isolation cooling (RCIC)
* Unit 2, reactor core isolation cooling (RCIC)
Line 95: Line 132:


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R05}}
{{a|1R05}}
 
==1R05 Fire Protection==
==1R05 Fire Protection


====a. Inspection Scope====
====a. Inspection Scope====
Quarterly Inspection (71111.05Q - 5 samples) The inspectors evaluated the adequacy of selected pre-fire plans by comparing the pre-fire plans to the defined hazards and defense-in-depth features specified in the fire protection program. In evaluating the pre-fire plans, the inspectors assessed the following items:
Quarterly Inspection (71111.05Q - 5 samples)  
 
==
The inspectors evaluated the adequacy of selected pre-fire plans by comparing the pre-fire plans to the defined hazards and defense-in-depth features specified in the fire protection program. In evaluating the pre-fire plans, the inspectors assessed the following items:
* control of transient combustibles and ignition sources
* control of transient combustibles and ignition sources
* fire detection systems
* fire detection systems
Line 108: Line 148:
* passive fire protection features
* passive fire protection features
* compensatory measures and fire watches
* compensatory measures and fire watches
* issues related to fire protection contained in the licensee's CAP   The inspectors toured the following fire areas to assess material condition and operational status of fire protection equipment. Documents reviewed are listed in the Attachment.
* issues related to fire protection contained in the licensees CAP  
 
The inspectors toured the following fire areas to assess material condition and operational status of fire protection equipment. Documents reviewed are listed in the  
.
* 2PFP-TB2-01A, Unit 2 Turbine Building Breezeway, North 20 foot elevation
* 2PFP-TB2-01A, Unit 2 Turbine Building Breezeway, North 20 foot elevation
* 2PFP-RB2-07, Unit 2 Drywell, 20 foot elevation
* 2PFP-RB2-07, Unit 2 Drywell, 20 foot elevation
Line 118: Line 161:
No findings were identified.
No findings were identified.


{{a|1R06}}
{{a|1R06}}
 
==1R06 Flood Protection Measures==
==1R06 Flood Protection Measures==
{{IP sample|IP=IP 71111.06|count=1}}
{{IP sample|IP=IP 71111.06|count=1}}


====a. Inspection Scope====
====a. Inspection Scope====
Underground Cables The inspectors reviewed related flood analysis documents and inspected the areas listed below containing cables whose failure could disable risk-significant equipment. The inspectors directly observed the condition of cables and cable support structures and, as applicable, verified that dewatering devices and drainage systems were functioning properly. In addition, the inspectors verified the licensee was identifying and properly addressing issues using the CAP. Documents reviewed are listed in the Attachment.
Underground Cables  
 
The inspectors reviewed related flood analysis documents and inspected the areas listed below containing cables whose failure could disable risk-significant equipment. The inspectors directly observed the condition of cables and cable support structures and, as applicable, verified that dewatering devices and drainage systems were functioning properly. In addition, the inspectors verified the licensee was identifying and properly addressing issues using the CAP. Documents reviewed are listed in the Attachment.
* Unit 2, manhole 2-MH-6NW, 2-MH-6SW
* Unit 2, manhole 2-MH-6NW, 2-MH-6SW


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No findings were identified.
No findings were identified.


{{a|1R11}}
{{a|1R11}}
 
==1R11 Licensed Operator Requalification Program and Licensed Operator Performance==
==1R11 Licensed Operator Requalification Program and Licensed Operator Performance==
{{IP sample|IP=IP 71111.11|count=2}}
{{IP sample|IP=IP 71111.11|count=2}}
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====a. Inspection Scope====
====a. Inspection Scope====
===.1 Resident Inspector Quarterly Review of Licensed Operator Requalification===
===.1 Resident Inspector Quarterly Review of Licensed Operator Requalification===
On June 1, 2017 the inspectors observed an evaluated simulator scenario, involving a NSW header leak and RCIC steam line break with failure to isolate, administered to an operating crew as part of the annual requalification operating test required by 10 CFR 55.59, "Requalification". The inspectors assessed the following:
On June 1, 2017 the inspectors observed an evaluated simulator scenario, involving a NSW header leak and RCIC steam line break with failure to isolate, administered to an operating crew as part of the annual requalification operating test required by 10 CFR 55.59, Requalification.
 
The inspectors assessed the following:
* licensed operator performance
* licensed operator performance
* the ability of the licensee to administer the scenario and evaluate the operators
* the ability of the licensee to administer the scenario and evaluate the operators
* the quality of the post-scenario critique
* the quality of the post-scenario critique
* simulator performance   Documents reviewed are listed in the Attachment.
* simulator performance  
 
Documents reviewed are listed in the Attachment.
 
===.2 Resident Inspector Quarterly Review of Licensed Operator Performance in the Actual===
Plant/Main Control Room


===.2 Resident Inspector Quarterly Review of Licensed Operator Performance in the Actual Plant/Main Control Room===
The inspectors observed licensed operator performance in the main control room on April 14, 2017, during plant startup from Unit 2 refueling outage B223R1.
The inspectors observed licensed operator performance in the main control room on April 14, 2017, during plant startup from Unit 2 refueling outage B223R1.


Line 151: Line 204:
* use of human error prevention techniques
* use of human error prevention techniques
* documentation of activities
* documentation of activities
* management and supervision Documents reviewed are listed in the Attachment.
* management and supervision  
 
Documents reviewed are listed in the Attachment.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.


{{a|1R12}}
{{a|1R12}}
 
==1R12 Maintenance Effectiveness==
==1R12 Maintenance Effectiveness==
{{IP sample|IP=IP 71111.12|count=1}}
{{IP sample|IP=IP 71111.12|count=1}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors assessed the licensee's treatment of the issues listed below to verify the licensee appropriately addressed equipment problems within the scope of the maintenance rule (10 CFR 50.65, "Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants"). The inspectors reviewed procedures and records to evaluate the licensee's identification, assessment, and characterization of the problems as well as their corrective actions for returning the equipment to a satisfactory condition. Documents reviewed are listed in the Attachment.
The inspectors assessed the licensees treatment of the issues listed below to verify the licensee appropriately addressed equipment problems within the scope of the maintenance rule (10 CFR 50.65, Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants). The inspectors reviewed procedures and records to evaluate the licensees identification, assessment, and characterization of the problems as well as their corrective actions for returning the equipment to a satisfactory condition. Documents reviewed are listed in the Attachment.
* WO 20132630, Unit 1 high pressure coolant injection (HPCI) auxiliary oil pump motor overload relay replacement
* WO 20132630, Unit 1 high pressure coolant injection (HPCI) auxiliary oil pump motor overload relay replacement


====b. Findings====
====b. Findings====
No findings were identified.  
No findings were identified.
{{a|1R13}}
 
{{a|1R13}}
 
==1R13 Maintenance Risk Assessments and Emergent Work Control==
==1R13 Maintenance Risk Assessments and Emergent Work Control==
{{IP sample|IP=IP 71111.13|count=4}}
{{IP sample|IP=IP 71111.13|count=4}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the maintenance activities listed below to verify that the licensee assessed and managed plant risk as required by 10 CFR 50.65(a)(4) and licensee procedures. The inspectors assessed the adequacy of the licensee's risk assessments and implementation of risk management actions. The inspectors also verified that the licensee was identifying and resolving problems with assessing and managing maintenance-related risk using the CAP. Additionally, for maintenance resulting from unforeseen situations, the inspectors assessed the effectiveness of the licensee's planning and control of emergent work activities. Documents reviewed are listed in the Attachment.
The inspectors reviewed the maintenance activities listed below to verify that the licensee assessed and managed plant risk as required by 10 CFR 50.65(a)(4) and licensee procedures. The inspectors assessed the adequacy of the licensees risk assessments and implementation of risk management actions. The inspectors also verified that the licensee was identifying and resolving problems with assessing and managing maintenance-related risk using the CAP. Additionally, for maintenance resulting from unforeseen situations, the inspectors assessed the effectiveness of the licensees planning and control of emergent work activities. Documents reviewed are listed in the Attachment.
* Unit 2, April 3, 2017, elevated risk during refueling outage B223R1 fuel movement
* Unit 2, April 3, 2017, elevated risk during refueling outage B223R1 fuel movement
* Unit 2, April 6, 2017, elevated risk during refueling outage B223R1 electrical work window
* Unit 2, April 6, 2017, elevated risk during refueling outage B223R1 electrical work window
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No findings were identified.
No findings were identified.


{{a|1R15}}
{{a|1R15}}
 
==1R15 Operability Determinations and Functionality Assessments==
==1R15 Operability Determinations and Functionality Assessments==
{{IP sample|IP=IP 71111.15|count=5}}
{{IP sample|IP=IP 71111.15|count=5}}


====a. Inspection Scope====
====a. Inspection Scope====
Operability and Functionality Review The inspectors selected the operability determinations or functionality evaluations listed below for review based on the risk-significance of the associated components and systems. The inspectors reviewed the technical adequacy of the determinations to ensure that TS operability was properly justified and the components or systems remained capable of performing their design functions. To verify whether components or systems were operable, the inspectors compared the operability and design criteria in the appropriate sections of the TS and updated final safety analysis report to the licensee's evaluations. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. Additionally, the inspectors reviewed a sample of corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with operability evaluations. Documents reviewed are listed in the Attachment.
Operability and Functionality Review  
* Unit 2, residual heat removal (RHR) valve F047B, heat exchanger 2B inlet valve, ground alarm, NCR 2113446
 
The inspectors selected the operability determinations or functionality evaluations listed below for review based on the risk-significance of the associated components and systems. The inspectors reviewed the technical adequacy of the determinations to ensure that TS operability was properly justified and the components or systems remained capable of performing their design functions. To verify whether components or systems were operable, the inspectors compared the operability and design criteria in the appropriate sections of the TS and updated final safety analysis report to the licensees evaluations. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. Additionally, the inspectors reviewed a sample of corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with operability evaluations. Documents reviewed are listed in the Attachment.
* Unit 2, residual heat removal (RHR) valve F047B, heat exchanger 2B inlet valve, ground alarm, NCR 2113446
* Unit 2, emergency diesel generators (EDG) 2 overspeed relay failure, NCR 2120738
* Unit 2, emergency diesel generators (EDG) 2 overspeed relay failure, NCR 2120738
* Unit 2, RCIC high moisture content in turbine oil, NCR 2126899
* Unit 2, RCIC high moisture content in turbine oil, NCR 2126899
Line 195: Line 256:
One licensee-identified violation was documented in Section 4OA7.
One licensee-identified violation was documented in Section 4OA7.


{{a|1R18}}
{{a|1R18}}
 
==1R18 Plant Modifications==
==1R18 Plant Modifications==
{{IP sample|IP=IP 71111.18|count=2}}
{{IP sample|IP=IP 71111.18|count=2}}
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The inspectors verified that the plant modifications listed below did not affect the safety functions of important safety systems. The inspectors confirmed the modifications did not degrade the design bases, licensing bases, and performance capability of risk significant SSCs. The inspectors also verified modifications performed during plant configurations involving increased risk did not place the plant in an unsafe condition.
The inspectors verified that the plant modifications listed below did not affect the safety functions of important safety systems. The inspectors confirmed the modifications did not degrade the design bases, licensing bases, and performance capability of risk significant SSCs. The inspectors also verified modifications performed during plant configurations involving increased risk did not place the plant in an unsafe condition.


Additionally, the inspectors evaluated whether system operability and availability, configuration control, post-installation test activities, and changes to documents, such as drawings, procedures, and operator training materials, complied with licensee standards and NRC requirements. In addition, the inspectors reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with modifications. Documents reviewed are listed in the Attachment.
Additionally, the inspectors evaluated whether system operability and availability, configuration control, post-installation test activities, and changes to documents, such as drawings, procedures, and operator training materials, complied with licensee standards and NRC requirements. In addition, the inspectors reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with modifications. Documents reviewed are listed in the  
* NCR 2124497, Carabiners installed for barring gear locking pins on EDGs 1, 2 and 3
.
* NCR 2124497, Carabiners installed for barring gear locking pins on EDGs 1, 2 and 3
* EC408181, Unit 2 RHR F047B, heat exchanger 2B inlet valve, motor replacement
* EC408181, Unit 2 RHR F047B, heat exchanger 2B inlet valve, motor replacement


====b. Findings====
====b. Findings====
No findings were identified.  
No findings were identified.
{{a|1R19}}
 
{{a|1R19}}
 
==1R19 Post-Maintenance Testing==
==1R19 Post-Maintenance Testing==
{{IP sample|IP=IP 71111.19|count=6}}
{{IP sample|IP=IP 71111.19|count=6}}
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* WO 20153997, Unit 1, service water backdraft damper lubrication, May 25, 2017
* WO 20153997, Unit 1, service water backdraft damper lubrication, May 25, 2017
* WO 20157390, Unit 2, RHR F047B, heat exchanger 2B inlet valve, motor replacement, May 30, 2017
* WO 20157390, Unit 2, RHR F047B, heat exchanger 2B inlet valve, motor replacement, May 30, 2017
* WO 20156298 , Unit 2, HPCI planned maintenance outage, June 14, 2017
* WO 20156298, Unit 2, HPCI planned maintenance outage, June 14, 2017
* WO 13538781, Units 1, EDG 2 planned maintenance outage, June 8, 2017 The inspectors evaluated these activities for the following:
* WO 13538781, Units 1, EDG 2 planned maintenance outage, June 8, 2017  
 
The inspectors evaluated these activities for the following:
* Acceptance criteria were clear and demonstrated operational readiness
* Acceptance criteria were clear and demonstrated operational readiness
* Effects of testing on the plant were adequately addressed
* Effects of testing on the plant were adequately addressed
Line 225: Line 292:
* Tests were performed in accordance with approved procedures
* Tests were performed in accordance with approved procedures
* Equipment was returned to its operational status following testing
* Equipment was returned to its operational status following testing
* Test documentation was properly evaluated Additionally, the inspectors reviewed a sample of corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with post-maintenance testing. Documents reviewed are listed in the Attachment.
* Test documentation was properly evaluated  
 
Additionally, the inspectors reviewed a sample of corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with post-maintenance testing. Documents reviewed are listed in the Attachment.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.


{{a|1R20}}
{{a|1R20}}
 
==1R20 Refueling and Other Outage Activities==
==1R20 Refueling and Other Outage Activities==
{{IP sample|IP=IP 71111.20|count=2}}
{{IP sample|IP=IP 71111.20|count=2}}
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===.1 Unit 2 Refueling Outage B223R1===
===.1 Unit 2 Refueling Outage B223R1===
{{IP sample|IP=IP 71111.20|count=1}}
{{IP sample|IP=IP 71111.20|count=1}}
Unit 2 began the inspection period in refueling outage B223R1. The inspectors reviewed outage plans and contingency plans for the Unit 2 refueling outage, which ended with the generator synchronization to the grid on April 15, 2017, to confirm that the licensee had appropriately considered risk, industry experience, and previous site-specific problems in developing and implementing a plan that assured maintenance of defense-in-depth of key safety functions. During the refueling outage, the inspectors monitored licensee controls over the following outage activities:
Unit 2 began the inspection period in refueling outage B223R1. The inspectors reviewed outage plans and contingency plans for the Unit 2 refueling outage, which ended with the generator synchronization to the grid on April 15, 2017, to confirm that the licensee had appropriately considered risk, industry experience, and previous site-specific problems in developing and implementing a plan that assured maintenance of defense-in-depth of key safety functions.
 
During the refueling outage, the inspectors monitored licensee controls over the following outage activities:
* Licensee configuration management, including maintenance of defense-in-depth for key safety functions and compliance with the applicable Technical Specifications (TSs) when taking equipment out of service
* Licensee configuration management, including maintenance of defense-in-depth for key safety functions and compliance with the applicable Technical Specifications (TSs) when taking equipment out of service
* Implementation of clearance activities and confirmation that tags were properly hung and equipment appropriately configured to safely support the work or testing
* Implementation of clearance activities and confirmation that tags were properly hung and equipment appropriately configured to safely support the work or testing
Line 248: Line 320:
* Maintenance of secondary containment as required by TS
* Maintenance of secondary containment as required by TS
* Startup and ascension to full power operation, tracking of startup prerequisites, walkdown of the drywell (primary containment) to verify that debris had not been left which could block emergency core cooling system suction strainers, and reactor physics testing
* Startup and ascension to full power operation, tracking of startup prerequisites, walkdown of the drywell (primary containment) to verify that debris had not been left which could block emergency core cooling system suction strainers, and reactor physics testing
* Licensee identification and resolution of problems related to refueling outage activities Documents reviewed are listed in the Attachment.
* Licensee identification and resolution of problems related to refueling outage activities  
 
Documents reviewed are listed in the Attachment.


===.2 Unit 1 Maintenance Outage B120F1===
===.2 Unit 1 Maintenance Outage B120F1===
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* developed work schedules to manage fatigue
* developed work schedules to manage fatigue
* developed mitigation strategies for loss of key safety functions
* developed mitigation strategies for loss of key safety functions
* adhered to operating license and TS requirements Inspectors verified that safety-related and risk-significant SSCs not accessible during power operations were maintained in an operable condition. The inspectors also reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with outage activities. Documents reviewed are listed in the Attachment.
* adhered to operating license and TS requirements  
 
Inspectors verified that safety-related and risk-significant SSCs not accessible during power operations were maintained in an operable condition. The inspectors also reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with outage activities. Documents reviewed are listed in the Attachment.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.


{{a|1R22}}
{{a|1R22}}
 
==1R22 Surveillance Testing==
==1R22 Surveillance Testing==
{{IP sample|IP=IP 71111.22|count=4}}
{{IP sample|IP=IP 71111.22|count=4}}
Line 274: Line 351:
The inspectors evaluated the test activities to assess for preconditioning of equipment, procedure adherence, and equipment alignment following completion of the surveillance.
The inspectors evaluated the test activities to assess for preconditioning of equipment, procedure adherence, and equipment alignment following completion of the surveillance.


Additionally, the inspectors reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with surveillance testing. Documents reviewed are listed in the Attachment. Routine Surveillance Tests
Additionally, the inspectors reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with surveillance testing. Documents reviewed are listed in the Attachment.
 
Routine Surveillance Tests
* Procedure 2MST-RPS41R, RPS Logic System Functional Test, April 6, 2017
* Procedure 2MST-RPS41R, RPS Logic System Functional Test, April 6, 2017
* Procedure 0PT-80.1, Reactor Pressure Vessel ASME Section XI Pressure Test, May 11, 2017 In-Service Tests (IST)
* Procedure 0PT-80.1, Reactor Pressure Vessel ASME Section XI Pressure Test, May 11, 2017  
* Procedure 0PT-09.2, HPCI System Operability Test, May 10, 2017   Reactor Coolant System Leak Detection
 
In-Service Tests (IST)
* Procedure 0PT-09.2, HPCI System Operability Test, May 10, 2017  
 
Reactor Coolant System Leak Detection
* Procedure 0OI-02.3, Unit 1 Drywell Leakage Control, April 25, 2017
* Procedure 0OI-02.3, Unit 1 Drywell Leakage Control, April 25, 2017


Line 283: Line 366:
No findings were identified.
No findings were identified.


===Cornerstone:===
===Cornerstone: Emergency Preparedness===
Emergency Preparedness
{{a|1EP6}}
{{a|1EP6}}
 
==1EP6 Drill Evaluation==
==1EP6 Drill Evaluation==
{{IP sample|IP=IP 71114.06|count=1}}
{{IP sample|IP=IP 71114.06|count=1}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors observed the emergency preparedness drill conducted on June 1, 2017, involving a NSW header leak and RCIC steam line break with failure to isolate. The inspectors observed licensee activities in the simulator and technical support center to evaluate implementation of the emergency plan, including event classification, notification, and protective action recommendations. The inspectors evaluated the licensee's performance against criteria established in the licensee's procedures. Additionally, the inspectors attended the post-exercise critique to assess the licensee's effectiveness in identifying emergency preparedness weaknesses and verified the identified weaknesses were entered in the CAP. Documents reviewed are listed in the  
The inspectors observed the emergency preparedness drill conducted on June 1, 2017, involving a NSW header leak and RCIC steam line break with failure to isolate. The inspectors observed licensee activities in the simulator and technical support center to evaluate implementation of the emergency plan, including event classification, notification, and protective action recommendations. The inspectors evaluated the licensees performance against criteria established in the licensees procedures.
 
Additionally, the inspectors attended the post-exercise critique to assess the licensees effectiveness in identifying emergency preparedness weaknesses and verified the identified weaknesses were entered in the CAP. Documents reviewed are listed in the  
.
.


Line 297: Line 382:


==OTHER ACTIVITIES==
==OTHER ACTIVITIES==
{{a|4OA1}}


{{a|4OA1}}
==4OA1 Performance Indicator (PI) Verification==
==4OA1 Performance Indicator (PI) Verification==
{{IP sample|IP=IP 71151|count=6}}
{{IP sample|IP=IP 71151|count=6}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed a sample of the performance indicator data, submitted by the licensee, for the Unit 1 and Unit 2 PIs listed below. The inspectors reviewed plant records compiled between April 1, 2016, through March 31, 2017, to verify the accuracy and completeness of the data reported for the station. The inspectors verified that the PI data complied with guidance contained in Nuclear Energy Institute 99-02, "Regulatory Assessment Performance Indicator Guideline," and licensee procedures. The inspectors verified the accuracy of reported data that were used to calculate the value of each PI. In addition, the inspectors reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with PI data. Documents reviewed are listed in the Attachment.
The inspectors reviewed a sample of the performance indicator data, submitted by the licensee, for the Unit 1 and Unit 2 PIs listed below. The inspectors reviewed plant records compiled between April 1, 2016, through March 31, 2017, to verify the accuracy and completeness of the data reported for the station. The inspectors verified that the PI data complied with guidance contained in Nuclear Energy Institute 99-02, Regulatory Assessment Performance Indicator Guideline, and licensee procedures. The inspectors verified the accuracy of reported data that were used to calculate the value of each PI.
 
In addition, the inspectors reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with PI data. Documents reviewed are listed in the Attachment.


===Cornerstone:===
===Cornerstone: Mitigating Systems===
Mitigating Systems
* Units 1 and 2, safety system functional failures
* Units 1 and 2, safety system functional failures
* Units 1 and 2, emergency AC power system
* Units 1 and 2, emergency AC power system
Line 314: Line 400:
No findings were identified.
No findings were identified.


{{a|4OA2}}
{{a|4OA2}}
 
==4OA2 Problem Identification and Resolution==
==4OA2 Problem Identification and Resolution==
{{IP sample|IP=IP 71152|count=2}}
{{IP sample|IP=IP 71152|count=2}}


===.1 Routine Review===
===.1 Routine Review===
The inspectors screened items entered into the licensee's corrective action program to identify repetitive equipment failures or specific human performance issues for follow-up.
The inspectors screened items entered into the licensees corrective action program to identify repetitive equipment failures or specific human performance issues for follow-up.


The inspectors reviewed condition reports, attended screening meetings, or accessed the licensee's computerized corrective action database.
The inspectors reviewed condition reports, attended screening meetings, or accessed the licensees computerized corrective action database.


===.2 Semi-Annual Trend Review===
===.2 Semi-Annual Trend Review===
====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed issues entered in the licensee's corrective action program and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors focused their review on human performance trends during Unit 2 refueling outage B223R1, but also considered the results of inspector daily condition report screenings, licensee trending efforts, and licensee human performance results. The review nominally considered the 6-month period of January 1, 2017, through June 30, 2017, although some examples extended beyond those dates when the scope of the trend warranted. The inspectors compared their results with the licensee's analysis of trends. Additionally, the inspectors reviewed the adequacy of corrective actions associated with a sample of the issues identified in the licensee's trend reports. The inspectors also reviewed corrective action documents that were processed by the licensee to identify potential adverse trends in the condition of structures, systems, and/or components as evidenced by acceptance of long-standing non-conforming or degraded conditions. Documents reviewed are listed in the  
The inspectors reviewed issues entered in the licensees corrective action program and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors focused their review on human performance trends during Unit 2 refueling outage B223R1, but also considered the results of inspector daily condition report screenings, licensee trending efforts, and licensee human performance results. The review nominally considered the 6-month period of January 1, 2017, through June 30, 2017, although some examples extended beyond those dates when the scope of the trend warranted. The inspectors compared their results with the licensees analysis of trends. Additionally, the inspectors reviewed the adequacy of corrective actions associated with a sample of the issues identified in the licensees trend reports. The inspectors also reviewed corrective action documents that were processed by the licensee to identify potential adverse trends in the condition of structures, systems, and/or components as evidenced by acceptance of long-standing non-conforming or degraded conditions. Documents reviewed are listed in the  
.
.


Line 333: Line 419:


===.3 Annual Follow-Up of Selected Issues===
===.3 Annual Follow-Up of Selected Issues===
====a. Inspection Scope====
====a. Inspection Scope====
The inspectors conducted a detailed review of the following condition report:
The inspectors conducted a detailed review of the following condition report:
* NCR 2120423, rising trend in Unit 2 suppression pool temperature, April 30, 2017 The inspectors evaluated the following attributes of the licensee's actions:
* NCR 2120423, rising trend in Unit 2 suppression pool temperature, April 30, 2017  
 
The inspectors evaluated the following attributes of the licensees actions:
* complete and accurate identification of the problem in a timely manner
* complete and accurate identification of the problem in a timely manner
* evaluation and disposition of operability and reportability issues
* evaluation and disposition of operability and reportability issues
Line 343: Line 430:
* identification of root and contributing causes of the problem
* identification of root and contributing causes of the problem
* identification of any additional condition reports
* identification of any additional condition reports
* completion of corrective actions in a timely manner Documents reviewed are listed in the Attachment.
* completion of corrective actions in a timely manner  
 
Documents reviewed are listed in the Attachment.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.


{{a|4OA3}}
{{a|4OA3}}
 
==4OA3 Follow-up of Events==
==4OA3 Follow-up of Events==
{{IP sample|IP=IP 71153|count=4}}
{{IP sample|IP=IP 71153|count=4}}


===.1 (Closed) Licensee Event Report (LER) 05000324/2017-001-00, Implementation of Enforcement Guidance Memorandum (EGM) 11-003, Revision 3===
===.1 (Closed) Licensee Event Report (LER) 05000324/2017-001-00, Implementation of===
Enforcement Guidance Memorandum (EGM) 11-003, Revision 3


====a. Inspection Scope====
====a. Inspection Scope====
On March 22, 2017, Unit 2 implemented the guidance of EGM 11-003, Revision 3, Enforcement Guidance Memorandum on Dispositioning Boiling Water Reactor Licensee Noncompliance with TS Containment Requirements During Operations with a Potential for Draining the Reactor Vessel. Consistent with this EGM, secondary containment operability was not maintained during operations with the potential for draining the reactor vessel activities. The EGM guidance was implemented from March 22, 2017, at 1209 to March 28, 2017, at 1230. The activities are discussed in Section 4OA5. Inspectors verified compliance with the guidelines of EGM 11-003 prior to and during these activities. The licensee has submitted a license amendment request to adopt TS Task Force traveler associated with generic resolution of this issue. The licensee entered this issue into the CAP as NCR 2110409. Documents reviewed are listed in the  
On March 22, 2017, Unit 2 implemented the guidance of EGM 11-003, Revision 3, Enforcement Guidance Memorandum on Dispositioning Boiling Water Reactor Licensee Noncompliance with TS Containment Requirements During Operations with a Potential for Draining the Reactor Vessel. Consistent with this EGM, secondary containment operability was not maintained during operations with the potential for draining the reactor vessel activities. The EGM guidance was implemented from March 22, 2017, at 1209 to March 28, 2017, at 1230. The activities are discussed in Section 4OA5.
 
Inspectors verified compliance with the guidelines of EGM 11-003 prior to and during these activities. The licensee has submitted a license amendment request to adopt TS Task Force traveler associated with generic resolution of this issue. The licensee entered this issue into the CAP as NCR 2110409. Documents reviewed are listed in the  
.
.


====b. Findings====
====b. Findings====
The enforcement actions associated with this LER are documented in Sections 4OA5.
The enforcement actions associated with this LER are documented in Sections 4OA5.
No findings were identified during the review of this LER. This LER is closed.
No findings were identified during the review of this LER. This LER is closed.


===.2 (Closed) LER 05000324/2017-002-00, Plant Mode Change with Primary Containment Inoperable===
===.2 (Closed) LER 05000324/2017-002-00, Plant Mode Change with Primary Containment===
Inoperable


====a. Inspection Scope====
====a. Inspection Scope====
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====b. Findings====
====b. Findings====
The enforcement actions associated with this LER are documented in Section 4OA7. No findings were identified during the review of this LER. This LER is closed.
The enforcement actions associated with this LER are documented in Section 4OA7.
No findings were identified during the review of this LER. This LER is closed.


===.3 (Closed) LER 05000325;324/2016-006-01, Control Room AC Units Inoperable Due to Corroded Supports===
===.3 (Closed) LER 05000325;324/2016-006-01, Control Room AC Units Inoperable Due to===
Corroded Supports


====a. Inspection Scope====
====a. Inspection Scope====
On December 14, 2016, the 2D control room AC unit was declared inoperable due to corrosion on the support channels, and Units 1 and 2 entered TS 3.7.4, Condition A. On January 30, 2017, the 1D control room AC unit was declared inoperable for corrosion on the support channels. The corrosion was due to trapped moisture in contact with steel supports exposed to a local marine environment. The corrosion degraded the supports to the point that the safety function of the AC unit would be lost during a seismic event.
On December 14, 2016, the 2D control room AC unit was declared inoperable due to corrosion on the support channels, and Units 1 and 2 entered TS 3.7.4, Condition A. On January 30, 2017, the 1D control room AC unit was declared inoperable for corrosion on the support channels. The corrosion was due to trapped moisture in contact with steel supports exposed to a local marine environment. The corrosion degraded the supports to the point that the safety function of the AC unit would be lost during a seismic event.


Since the degradation was due to corrosion, both units were determined to be inoperable at the same time. The conditions were determined to have existed longer than the TS 3.7.4 allowed outage time. The licensee entered this issue into the CAP as NCRs 2113799 and 2113800. As corrective actions, the licensee replaced both AC units' supports, declared the units operable, and inspected the 2E control room AC unit for corrosion.
Since the degradation was due to corrosion, both units were determined to be inoperable at the same time. The conditions were determined to have existed longer than the TS 3.7.4 allowed outage time. The licensee entered this issue into the CAP as NCRs 2113799 and 2113800. As corrective actions, the licensee replaced both AC units supports, declared the units operable, and inspected the 2E control room AC unit for corrosion.


====b. Findings====
====b. Findings====
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No additional findings were identified during the review of this LER. This LER is closed.
No additional findings were identified during the review of this LER. This LER is closed.


===.4 (Closed) LER 05000325;324/2017-002, Foreign Material in Switch Results in Unplanned Automatic Start of Emergency Diesel Generators===
===.4 (Closed) LER 05000325;324/2017-002, Foreign Material in Switch Results in Unplanned===
Automatic Start of Emergency Diesel Generators


====a. Inspection Scope====
====a. Inspection Scope====
Line 395: Line 491:
No findings were identified.
No findings were identified.


{{a|4OA5}}
{{a|4OA5}}
 
==4OA5 Other Activities==
==4OA5 Other Activities==
 
===.1 Implementation of EGM 11-003, Revision 3, Enforcement Guidance Memorandum on===
===.1 Implementation of EGM 11-003, Revision 3, Enforcement Guidance Memorandum on Dispositioning Boiling Water Reactor Licensee Noncompliance with Technical Specification Containment Requirements During Operations with a Potential for Draining the Reactor Vessel===
Dispositioning Boiling Water Reactor Licensee Noncompliance with Technical Specification Containment Requirements During Operations with a Potential for Draining the Reactor Vessel


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the plant's implementation of NRC EGM 11-003, Revision 3, during Unit 2 maintenance activities for operations with a potential for draining the reactor vessel (OPDRVs), during the Unit 2 refueling outage. Inspectors verified that for all dates, all other TS requirements were met during OPDRVs with secondary containment inoperable. Documents reviewed are listed in the Attachment.
The inspectors reviewed the plants implementation of NRC EGM 11-003, Revision 3, during Unit 2 maintenance activities for operations with a potential for draining the reactor vessel (OPDRVs), during the Unit 2 refueling outage. Inspectors verified that for all dates, all other TS requirements were met during OPDRVs with secondary containment inoperable. Documents reviewed are listed in the Attachment.


====b. Findings====
====b. Findings====
=====Description.=====
=====Description.=====
During the Unit 2 refueling outage, the OPDRVs activities are listed below:
During the Unit 2 refueling outage, the OPDRVs activities are listed below:
* March 21, 2017: 6 gallons per minute leakage for maintenance associated with the 2B recirculation pump seal rebuild
* March 21, 2017: 6 gallons per minute leakage for maintenance associated with the 2B recirculation pump seal rebuild
* March 23, 2017: 48 gallons per minute leakage for hydraulic control unit draining to support rod maintenance
* March 23, 2017: 48 gallons per minute leakage for hydraulic control unit draining to support rod maintenance
* March 24, 2017: 65 gallons per minute leakage to close the excess flow check valve and cap the drain line
* March 24, 2017: 65 gallons per minute leakage to close the excess flow check valve and cap the drain line
* March 27, 2017: 71.2 gallons per minute leakage to replace the low power range monitors and intermediate power range monitors   These activities took place without secondary containment being operable.
* March 27, 2017: 71.2 gallons per minute leakage to replace the low power range monitors and intermediate power range monitors  
 
These activities took place without secondary containment being operable.


=====Enforcement.=====
=====Enforcement.=====
TS 3.6.4.1, Secondary Containment, requires that secondary containment be operable and is applicable during OPDRVs. The required action if secondary containment is inoperable in this condition is to initiate actions to suspend OPDRVs immediately. Contrary to the above, on March 21, 2017, March 23, 2017, March 24, 2017, and March 27, 2017, the licensee failed to maintain secondary containment operable while performing OPDRVs.
TS 3.6.4.1, Secondary Containment, requires that secondary containment be operable and is applicable during OPDRVs. The required action if secondary containment is inoperable in this condition is to initiate actions to suspend OPDRVs immediately. Contrary to the above, on March 21, 2017, March 23, 2017, March 24, 2017, and March 27, 2017, the licensee failed to maintain secondary containment operable while performing OPDRVs.


However, because the violations were identified during the discretion period described in EGM 11-003, Revision 3, and the licensee met the criteria established in the EGM prior to and during these activities, the NRC exercised enforcement discretion (Enforcement Action-17-123) for the dates of March 21, 2017, March 23, 2017, March 24, 2017, and March 27, 2017, in accordance with Section 3.5, "Violations Involving Special Circumstances," of the NRC Enforcement Policy and, therefore, will not issue enforcement action for this violation. The inspectors observed that Brunswick has already submitted a license amendment request (BSEP 17-0060) on June 29, 2017 which was accepted for review by the NRC on July 18, 2017. The licensee entered this issue into the CAP as NCR 2110409.
However, because the violations were identified during the discretion period described in EGM 11-003, Revision 3, and the licensee met the criteria established in the EGM prior to and during these activities, the NRC exercised enforcement discretion (Enforcement Action-17-123) for the dates of March 21, 2017, March 23, 2017, March 24, 2017, and March 27, 2017, in accordance with Section 3.5, Violations Involving Special Circumstances, of the NRC Enforcement Policy and, therefore, will not issue enforcement action for this violation. The inspectors observed that Brunswick has already submitted a license amendment request (BSEP 17-0060) on June 29, 2017 which was accepted for review by the NRC on July 18, 2017. The licensee entered this issue into the CAP as NCR 2110409.


{{a|4OA6}}
{{a|4OA6}}
==4OA6 Meetings, Including Exit==
==4OA6 Meetings, Including Exit==
On July 12, 2017, the resident inspectors presented the inspection results to Mr. Gideon and other members of the licensee's staff. The inspectors verified that no proprietary information was retained by the inspectors or documented in this report.
On July 12, 2017, the resident inspectors presented the inspection results to Mr. Gideon and other members of the licensees staff. The inspectors verified that no proprietary information was retained by the inspectors or documented in this report.


{{a|4OA7}}
{{a|4OA7}}
==4OA7 Licensee Identified Violations==
==4OA7 Licensee Identified Violations==
The following violation of very low safety significance (Green) was identified by the licensee and is a violation of NRC requirements which meet the criteria of the NRC Enforcement Policy, for being dispositioned as a non-cited violation.
The following violation of very low safety significance (Green) was identified by the licensee and is a violation of NRC requirements which meet the criteria of the NRC Enforcement Policy, for being dispositioned as a non-cited violation.
* LCO 3.0.4 states, in part, when an LCO is not met, entry into a MODE or other specified condition in the applicability shall only be made when the associated ACTIONS to be entered permit continued operation in the MODE for an unlimited period of time. Contrary to the above, on April 13, 2017, at 2347, the licensee changed modes on Unit 2 from Mode 4 to Mode 2 with the primary containment inoperable. Specifically, TS 3.6.1.1, Primary Containment, requires primary containment to be operable in Modes 1, 2, and 3, however, the reactor was taken to Mode 2 with the primary containment still aligned for venting. In this condition, the drywell ventilation makes the primary containment inoperable due to the drywell and the suppression chamber being in communication to each other. This condition is allowed for two hours before the required action to shutdown to Mode 4 is required. Since the required action is not permitted for continued operation, a violation of LCO 3.0.4 occurred. The cause of the event was the failure of operations personnel to initiate a tracking LCO for primary containment being inoperable in accordance with licensee procedure 0OI-01.01, BNP Conduct of Operations Supplement. The licensee determined a tracking LCO should have been initiated to ensure the primary containment was restored to operable prior to entering Mode 2. As immediate corrective actions, the licensee restored containment to operable on April 14, 2017, at 0030, and the Shift Manager and Control Room Supervisor were removed from shift. Further, a remediation plan was developed and implemented to assess the Shift Manager and Control Room Supervisor for watch standing and reinstatement.
* LCO 3.0.4 states, in part, when an LCO is not met, entry into a MODE or other specified condition in the applicability shall only be made when the associated ACTIONS to be entered permit continued operation in the MODE for an unlimited period of time.
 
Contrary to the above, on April 13, 2017, at 2347, the licensee changed modes on Unit 2 from Mode 4 to Mode 2 with the primary containment inoperable. Specifically, TS 3.6.1.1, Primary Containment, requires primary containment to be operable in Modes 1, 2, and 3, however, the reactor was taken to Mode 2 with the primary containment still aligned for venting. In this condition, the drywell ventilation makes the primary containment inoperable due to the drywell and the suppression chamber being in communication to each other. This condition is allowed for two hours before the required action to shutdown to Mode 4 is required. Since the required action is not permitted for continued operation, a violation of LCO 3.0.4 occurred. The cause of the event was the failure of operations personnel to initiate a tracking LCO for primary containment being inoperable in accordance with licensee procedure 0OI-01.01, BNP Conduct of Operations Supplement. The licensee determined a tracking LCO should have been initiated to ensure the primary containment was restored to operable prior to entering Mode 2. As immediate corrective actions, the licensee restored containment to operable on April 14, 2017, at 0030, and the Shift Manager and Control Room Supervisor were removed from shift. Further, a remediation plan was developed and implemented to assess the Shift Manager and Control Room Supervisor for watch standing and reinstatement.


This finding is associated with the Barrier Integrity Cornerstone. Using IMC 0609, Appendix G, Shutdown Operations Significance Determination Process, 1, Exhibit 4, Barrier Integrity Screening Questions, the finding screened to Green because it did not degrade the ability to close or isolate the containment, it did not degrade the physical integrity of reactor containment, and it did not involve an actual reduction in function of hydrogen control. This issue was documented in the licensee's CAP as NCR 2116753.
This finding is associated with the Barrier Integrity Cornerstone. Using IMC 0609, Appendix G, Shutdown Operations Significance Determination Process, 1, Exhibit 4, Barrier Integrity Screening Questions, the finding screened to Green because it did not degrade the ability to close or isolate the containment, it did not degrade the physical integrity of reactor containment, and it did not involve an actual reduction in function of hydrogen control. This issue was documented in the licensees CAP as NCR 2116753.


ATTACHMENT:
ATTACHMENT:  


=SUPPLEMENTAL INFORMATION=
=SUPPLEMENTAL INFORMATION=


==KEY POINTS OF CONTACT==
==KEY POINTS OF CONTACT==
===Licensee Personnel===
K. Allen
Director, Design Engineering
B. Bagwell
Environmental & Chemistry
A. Baker
Supervisor, Environmental & Chemistry
J. Berry
Supervisor, LOCT Training
A. Brittain
Director, Nuclear Plant Security
P. Brown
Manager, Nuclear Performance Improvement
B. Bryant
Manager, Nuclear Oversight
J. Bryant
Regulatory Affairs
R. Carpenter
Radiation Monitor Engineer
P. Dubrouillet
Director, Nuclear Engineering, Mechanical Systems
C. Dunsmore
Manager, Nuclear Outage
W. Gideon
Vice President
L. Grzeck
Manager, Nuclear Regulatory Affairs
J. Hicks
Manager, Nuclear Training
B. Houston
Manager, Nuclear Maintenance
J. Johnson
Manager, Nuclear Chemistry
K. Krueger
Manager, Nuclear Operations
J. McAdoo
Manager, Nuclear Rad Protection
K. Moser
B. Murray
Plant Manager
Licensing
J. Nolin
General Manager, Nuclear Engineering
W. Orlando
Superintendent, E/I&C
O. Paladiy
Welding Engineer/Repair & Replacement Engineer
A. Padleckas
Assistant Ops Manager, Training
D. Petrusic
Superintendent, Environmental & Chemistry
J. Pierce
Manager, Nuclear Work Management
E. Rau
Operations Training
M. Regan
Project Manager, Major Projects
L. Rohrbaugh
Operator Training
M. Smiley
Manager, Nuclear Ops Training
L. Spencer
Operator Training
R. Wiemann
Director, Nuclear Engineering, Electrical Reactor Systems
E. Williams
Operations Manager
S. Williams
BWRVIP Program Engineer
C. Winslow
ISI Program Engineer
B. Wonton
Director, Nuclear Organizational Effectiveness


===Licensee Personnel===
State of North Carolina
: [[contact::K. Allen Director]], Design Engineering
 
: [[contact::B. Bagwell Environmental & Chemistry A. Baker Supervisor]], Environmental & Chemistry
P. Cox
: [[contact::J. Berry Supervisor]], LOCT Training
Department of Health and Human Services
: [[contact::A. Brittain Director]], Nuclear Plant Security
: [[contact::P. Brown Manager]], Nuclear Performance Improvement
: [[contact::B. Bryant Manager]], Nuclear Oversight J. Bryant Regulatory Affairs R. Carpenter Radiation Monitor Engineer
: [[contact::P. Dubrouillet Director]], Nuclear Engineering, Mechanical Systems
: [[contact::C. Dunsmore Manager]], Nuclear Outage
: [[contact::W. Gideon Vice President L. Grzeck Manager]], Nuclear Regulatory Affairs
: [[contact::J. Hicks Manager]], Nuclear Training
: [[contact::B. Houston Manager]], Nuclear Maintenance 
: [[contact::J. Johnson Manager]], Nuclear Chemistry
: [[contact::K. Krueger Manager]], Nuclear Operations
: [[contact::J. McAdoo Manager]], Nuclear Rad Protection
: [[contact::K. Moser  B. Murray Plant Manager Licensing J. Nolin General Manager]], Nuclear Engineering
: [[contact::W. Orlando Superintendent]], E/I&C
O. Paladiy Welding Engineer/Repair & Replacement Engineer
: [[contact::A. Padleckas Assistant Ops Manager]], Training
: [[contact::D. Petrusic Superintendent]], Environmental & Chemistry
: [[contact::J. Pierce Manager]], Nuclear Work Management
E. Rau Operations Training
: [[contact::M. Regan Project Manager]], Major Projects
: [[contact::L. Rohrbaugh Operator Training M. Smiley Manager]], Nuclear Ops Training L. Spencer Operator Training
: [[contact::R. Wiemann Director]], Nuclear Engineering, Electrical Reactor Systems
E. Williams Operations Manager
: [[contact::S. Williams BWRVIP Program Engineer C. Winslow ISI Program Engineer B. Wonton Director]], Nuclear Organizational Effectiveness


State of North Carolina  P. Cox Department of Health and Human Services 
===NRC Personnel===
===NRC Personnel===
: [[contact::S. Rose Chief]], Reactor Projects Branch 4  
S. Rose
: [[contact::P. Niebaum Acting Chief]], Reactor Projects Branch 4
Chief, Reactor Projects Branch 4
P. Niebaum
Acting Chief, Reactor Projects Branch 4  


==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==
==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==
===Opened and Closed===
===Opened and Closed===
: 05000324/2017-001-00   LER  Implementation of Enforcement Guidance Memorandum (EGM) 11-003, Revision 3
: 05000324/2017-001-00  
(Section 4OA3.1)
: 05000324/2017-002-00 LER Plant Mode Change with Primary Containment Inoperable (Section 4OA3.2) 
: 05000325;324/2016-006-01  LER  Control Room AC Units Inoperable Due to Corroded Supports (Section 4OA3.3) 
: 05000325;324/2017-002  LER  Foreign Material in Switch Results in Unplanned
Automatic Start of Emergency Diesel Generators 
(Section 4OA3.4)     


==LIST OF DOCUMENTS REVIEWED==
LER
Common Documents Reviewed Updated Final Safety Analysis Report Individual Plant Examination Individual Plant Examination of External Events Technical Specifications and Bases Technical Requirements Manual Control Room Narrative Logs Plan of the Day


==Section 1R01: Adverse Weather Protection Procedures==
Implementation of Enforcement Guidance Memorandum (EGM) 11-003, Revision 3 (Section 4OA3.1)
: 0AP-062, Seasonal Preparations, Rev. 6
: 05000324/2017-002-00 LER Plant Mode Change with Primary Containment Inoperable (Section 4OA3.2)
: AD-WC-ALL-0230, Seasonal Readiness, Rev. 0
: 05000325;324/2016-006-01
===Condition Report===
: 2122700
: Work Order 20147068


==Section 1R04: Equipment Alignment Procedures 2OP-18, Core Spray System Operating Procedure, Rev. 73 1OP-18, Core Spray System Operating Procedure, Rev. 61==
LER
: AD-EG-ALL-1615, Cable Aging Management Program, Rev. 0
: 1OP-43, Service Water Operating Procedure, Rev. 128 
===Condition Report===
: 2133573
: Work Order
: 20010900 
===Drawings===
: D-02524, Reactor Building Core Spray System Piping Diagram Sheet 1, Rev. 43 D-25024, Reactor Building Core Spray System Piping Diagram Sheet 2, Rev. 39
: D-20041, Service Water System Piping Diagram, Rev. 56


==Section 1R05: Fire Protection Procedures 2PFP-TB, Turbine Building Pre-Fire Plans, Rev. 31 2PFP-RB, Reactor Building PreFire Plans, Rev. 21==
Control Room AC Units Inoperable Due to Corroded Supports (Section 4OA3.3)
: 0PFP-DG, Diesel Generator Building PreFire Plan, Rev. 26
: 05000325;324/2017-002


==Section 1R06: Flood Protection Procedure==
LER
: EGR-NGGC-0512, Licensee Renewal Aging Management Activities, Rev. 8
===Condition Report===
: 2123053 
===Work Orders===
: 20030212 20030213


==Section 1R11: Licensed Operator Requalification Program and Licensed Operator Performance Procedures==
Foreign Material in Switch Results in Unplanned Automatic Start of Emergency Diesel Generators (Section 4OA3.4)
: LORX-037, NSW Header leak, RCIC steam line break with failure to isolate, Rev. 2 0GP-01, Pre-startup Checklist, Rev. 192 0GP-02, Approach to Criticality and Pressurization of the Reactor, Rev. 110
: 0GP-03, Unit Startup and Synchronization, Rev. 84
: 0GP-07, Preparations for Core Alterations, Rev. 63
: 0GP-12, Power Changes, Rev. 78 1PT-01.7, Heatup/Cooldown monitoring, Rev. 10 0OI-01.01, BNP Conduct of Operations Supplement, Rev. 82
: 0ENP-24.0, Reactor Engineering Guidelines, Rev. 67
: 0AP-022, BNP Outage Risk Management, Rev. 56
: 0ENP-24.13, Core Verification, Rev. 22


==Section 1R12: Maintenance Effectiveness Condition Reports
==LIST OF DOCUMENTS REVIEWED==
: 2123476 2043067==
 
===Work Orders===
: 20132630
 
==Section 1R13: Maintenance Risk Assessment and Emergent Work Control Procedures==
: AD-OP-ALL-0201, Protected Equipment, Rev. 04 0AP-022, BNP Outage Risk Management, Rev. 56
: AD-WC-ALL-0250, Work Implementation and Completion, Rev. 04
: AD-WC-ALL-0410, Work Activity Integrated Risk Management, Rev. 03
: AD-WC-ALL-0200, Online Work Management, Rev. 08
: AD-OP-ALL-0201, Protected Equipment, Rev. 04
: AD-WC-ALL-0430, Outage Risk Review, Rev. 02 0AP-025, BNP Integrated Scheduling, Rev. 56
===Condition Report===
: 2124169
: Work Order
: 20072392
===Miscellaneous===
: BNP Outage Risk Assessment
: BNP U2 Key Safety Function Daily Risk Assessment EOOS Risk Assessments
: BNP-PSA-041, BNP On-Line Equipment Out of Service Probabilistic Safety Assessment Model
 
==Section 1R15: Operability Determinations and Functionality Assessments Procedures==
: AD-OP-ALL-0105, Operability Determinations and Functionality Assessments, Rev. 3
===Condition Reports===
: 2116753
: 2120738
: 2121027
: 2126899
: 2113446
: 2127691
===Work Orders===
: 20163781
: 12086324 
===Miscellaneous===
: PDO CR2120738
 
==Section 1R18: Plant Modifications Procedures==
: AD-EG-ALL-1137, Engineering Change Product Selection, Rev. 3
: AD-EG-ALL-1138, Standard Design Process, Rev. 0
: AD-EG-ALL-1132, Preparation and Control of Design Change Engineering Changes, Rev. 6
: AD-EG-ALL-1117, Design Analyses and Calculations, Rev. 4 
===Condition Reports===
: 2113446
: 2124497 
===Miscellaneous===
: EC408181, RHR F047B motor replacement
 
==Section 1R19: Post Maintenance Testing Procedures 0PT-02.3.2, Reactor Building to Suppression Chamber Vacuum Breaker and Valve Operability Test, Rev. 33==
: 0PT-12.2B, No. 2 Diesel Generator Monthly Load Test, Rev. 109 
===Condition Reports===
: 2124169
: 2116038
: 2113066
: 2113446
: 2131762
: 2130937
: 2131688
===Work Orders===
: 20072392
: 20156990
: 20156298
: 20153997
: 20096176
: 13538781
===Miscellaneous===
: Calculation 0SWB-006 Rev 0
: Apparent Cause Evaluation
: 211038
: EC 296474, EDG Governor Replacement Modification
 
==Section 1R20: Refueling and Other Outage Activities Procedures 0GP-01, Pre-startup Checklist, Rev. 192 0GP-02, Approach to Criticality and Pressurization of the Reactor, Rev. 110==
: 0GP-03, Unit Startup and Synchronization, Rev. 84 0GP-05, Unit Shutdown, Rev. 182 0GP-07, Preparations for Core Alterations, Rev. 63
: 0GP-12, Power Changes, Rev. 78
: 1PT-01.7, Heatup/Cooldown monitoring, Rev. 10
: 0OI-01.01, BNP Conduct of Operations Supplement, Rev. 82 0OI-01.06, Post Trip Review, Rev. 46 0MMM-015, Operation and Inspection of Cranes and Material Handling Equipment, Rev. 67
: 0ENP-24.0, Reactor Engineering Guidelines, Rev. 67 0AP-022, BNP Outage Risk Management, Rev. 56 0ENP-24.13, Core Verification, Rev. 22
: 2SP-15-101, Unit 2
: EGM 11-003 OPDRV Activities, Rev. 1 
===Condition Reports===
: 2109110
: 2109091
: 2108800
: 2108718
: 2111148
: 2111542
: 2111474
: 2115107
: 2115089
: 2115088
: 2115035
: 2114985
: 2114833
: 2105377
: 2099005 
===Work Orders===
: 20074532
: 11904847
: 2158321
===Miscellaneous===
: Daily Outage Reports Daily Key Safety Function Status Sheets Daily Risk Profiles Crew Turnover Reports Fatigue Rule Management List of Operations with the Potential for Draining the Reactor Vessel (OPDRVs)
: Mode Change Checklists Progress Reporter Schedule Outage Risk Assessment
: NRC
: EGM 11-003, Rev. 3, Dispositioning Boiling Water Reactor Licensee Noncompliance with Technical Specification Containment Requirements during OPDRVs Operator Logs List of Outage Modifications Core Verification Videos
 
==Section 1R22: Surveillance Testing==
 
===Procedures===
: 0PT-80.1, Reactor Pressure Vessel ASME Section XI Pressure Test, Rev. 70 
: 0OI-02.3, Drywell Leakage Control, Rev.7 2MST-RPS41R, RPS Logic System Functional Test, Rev. 24 0PT-09.2, HPCI System Operability Test, Rev. 148
 
==Section 1EP6: Drill Evaluation==
 
===Procedures===
: 0OI-01.07, Notifications, Rev. 38 2EOP-01-RSP, Reactor Scram Procedure, Rev. 16
: 0PEP-02.1, Initial Emergency Actions, Rev. 53
: 0PEP-02.1.1, Emergency Control - Notification of Unusual Event, Alert, Site Area Emergency, and General Emergency, Rev. 29
: LORX-037, NSW Header leak and RCIC steam line break with failure to isolate, Rev. 2
 
==Section 4OA1: Performance Indicator Verification Procedures==
: AD-LS-ALL-0004. Performance Indicators and Monthly Operating Report, Rev. 01
===Miscellaneous===
: Operator Logs
: NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Rev. 7
: Brunswick Unit 1 PI Summary, April 1, 2016, through March 31, 2017
: Brunswick Unit 2 PI Summary, April 1, 2016, through March 31, 2017
: Monthly PI Reports, April 1, 2016, through March 31, 2017
: System Health Reports, April 1, 2016, through March 31, 2017 Licensee Event Reports, April 1, 2016, through March 31, 2017
 
==Section 4OA2: Problem Identification and Resolution Procedures==
: AD-HU-ALL-0001, Human Performance Program, Rev. 11
: AD-PI-ALL-0100, Corrective Action Program, Rev. 7
: AD-SY-ALL-0401, Fitness for Duty Program, Rev. 1
: AD-SY-ALL-0460, Managing Fatigue and Work Hour Limits, Rev. 1
: AD-SY-ALL-1000, Conduct of Security, Rev. 2
: AD-SY-ALL-0520, Security Training, Rev. 1
: SEC-NGGC-2141, Fitness for Duty Unscheduled Work Call Outs, Rev.11
: SEC-NGGC-2166, Security Access Controls, Rev. 15
: AD-PI-ALL-0101, Root Cause Evaluation, Rev. 4
: AD-PI-ALL-0102, Apparent Cause Evaluation, Rev. 4
: AD-PI-ALL-0103, Quick Cause Evaluation, Rev. 4
: AD-PI-ALL-0400, Operating Experience Program, Rev. 4
===Condition Reports===
: 2118029
: 2111095
: 2113981
: 2114013
: 2114985
: 2115269
: 2115331
: 2115577
: 2115822
: 2116631
: 2116753
: 2120423
===Miscellaneous===
: EC 266023
: Unit 2 Suppression Temperature Rising Trend
 
==Section 4OA3: Follow-up of Events==
 
===Procedures===
: AD-WC-ALL-0210, Work Request Initiation, Screening, Prioritization, and Classification, Rev. 7 2SP-15-101, Unit 2
: EGM 11-003 OPDRV Activities, Rev. 1
: 0OI-01.07, Notifications, Rev. 38
===Condition Reports===
: 2113799
: 2113800
: 2095663
: 2116753
: 2110409
: 2117033 
===Work Orders===
: 20132955
: 20068598
: 20160330 
===Miscellaneous===
: LER 05000324/2017-001-00, Implementation of Enforcement Guidance
: Memorandum (EGM)
: 11-003, Revision 3
: LER 05000324/2017-002-00, Plant Mode Change with Primary Containment Inoperable
: LER 05000325;324/2016-006-01, Control Room AC Units Inoperable Due to Corroded Supports Section 4OA5 : Other Activities
===Procedures===
: 2SP-15-10R, Unit 2
: EGM 11-003 OPDRV Activities, Rev. 1
===Condition Reports===
: 2110409
===Work Orders===
: Miscellaneous
: LER 05000324/2017-001-00, Implementation of Enforcement Guidance
: Memorandum (EGM)
: 11-003, Revision 3


==Section 4OA7: Licensee Identified Violations Procedures Procedure 0OI-01.01,==
: BNP Conduct of Operations Supplement, Rev. 82
===Condition Reports===
: 2116753
===Miscellaneous===
: Records
: LER 05000324/2017-002-00, Plant Mode Change with Primary Containment
}}
}}

Latest revision as of 15:55, 8 January 2025

NRC Integrated Inspection Report Nos. 05000325/2017002 and 05000324/2017002 and Exercise of Enforcement Discretion
ML17212A137
Person / Time
Site: Brunswick  Duke Energy icon.png
Issue date: 07/31/2017
From: Steven Rose
NRC/RGN-II/DRP/RPB4
To: William Gideon
Duke Energy Progress
References
EA-17-123 IR 2017002
Download: ML17212A137 (27)


Text

July 31, 2017

SUBJECT:

BRUNSWICK STEAM ELECTRIC PLANT - NRC INTEGRATED INSPECTION REPORT NOS.: 05000325/2017002 AND 05000324/2017002 AND EXERCISE OF ENFORCEMENT DISCRETION

Dear Mr. Gideon:

On June 30, 2017, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Brunswick Steam Electric Plant, Units 1 and 2. On July 12, 2017, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.

A violation of Technical Specification 3.6.4.1, Secondary Containment, was identified. Because the violation was identified during the discretion period described in Enforcement Guidance Memorandum 11-003, Revision 3, the NRC is exercising enforcement discretion in accordance with Section 3.5, Violations Involving Special Circumstances, of the NRC Enforcement Policy and, therefore, will not issue enforcement action for this violation, subject to the license amendment request which was submitted on June 29, 2017.

Further, inspectors documented a licensee-identified violation which was determined to be of very low safety significance in this report. The NRC is treating this violation as non-cited violation (NCV) consistent with Section 2.3.2.a of the Enforcement Policy.

If you contest the violation or the significance of the violation, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator Region II; the Director, Office of Enforcement, and the NRC Resident Inspector at the Brunswick Steam Electric Plant. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Steven D. Rose, Chief Reactor Projects Branch 4 Division of Reactor Projects

Docket Nos.: 50-325, 50-324 License Nos.: DPR-71, DPR-62

Enclosure:

IR 05000325, 324/2017002 w/Attachment: Supplementary Information

REGION II==

Docket Nos.:

50-325, 50-324

License Nos.:

DPR-71, DPR-62

Report No.:

05000325/2017002, 05000324/2017002

Licensee:

Duke Energy Progress, Inc.

Facility:

Brunswick Steam Electric Plant, Units 1 & 2

Location:

Southport, NC

Dates:

April 1, 2017 through June 30, 2017

Inspectors:

M. Catts, Senior Resident Inspector M. Schwieg, Resident Inspector D. Jackson, RII Project Engineer

Approved by:

Steven D. Rose, Chief Reactor Projects Branch 4

Division of Reactor Projects

SUMMARY

Integrated Inspection Report 05000325/2017002, 05000324/2017002; April 1, 2017, through

June 30, 2017; Brunswick Steam Electric Plant, Units 1 and 2.

The report covered a 3-month period of inspection by resident inspectors and regional inspectors. There were no NRC-identified or self-revealing violations documented in this report.

The significance of inspection findings are indicated by their color (i.e., greater than Green, or Green, White, Yellow, Red) and determined using Inspection Manual Chapter (IMC) 0609,

Significance Determination Process, (SDP) dated April 29, 2015. All violations of NRC requirements are dispositioned in accordance with the NRCs Enforcement Policy dated November 1, 2016. The NRCs program for overseeing the safe operations of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 6.

One violation of very low safety significance that was identified by the licensee has been reviewed by the NRC. Corrective action taken or planned by the licensee has been entered into the licensees corrective action program (CAP). This violation and corrective action tracking number is listed in Section 4OA7 of this report.

REPORT DETAILS

Summary of Plant Status

Unit 1 began the inspection period at 100 percent rated thermal power (RTP). On April 25, 2017, the unit was shut down for a forced outage to repair the 1B recirculation pump seal. On April 28, 2017, the unit was restarted and power was returned to 100 percent on May 1, 2017. On May 2, 2017, power was reduced to 66 percent for a control rod improvement and power was returned to 100 percent on May 4, 2017. On May 6, 2017, power was reduced to 80 percent for a control rod improvement and power was returned to 100 percent on May 8, 2017. On May 31, 2017, power was reduced to 98 percent due to a loss of the 1B variable frequency device controller for the 1B recirculation pump. Power was returned to 100 percent after restoration of the 1B variable frequency device controller on May 31, 2017.

On June 9, 2017, power was reduced to 70 percent for a control rod improvement and power was returned to 100 percent on June 11, 2017. The unit remained at or near 100 percent RTP for the remainder of the inspection period.

Unit 2 began the inspection period shutdown for refueling outage B223R1. On April 14, 2017, the unit was restarted and power was returned to 100 percent on April 22, 2017. On May 22, 2017, power was reduced to 70 percent to repair a steam leak on 2-MD-V16 and power was returned to 100 percent on May 22, 2017. On June 3, 2017, power was reduced to 70 percent for a control rod sequence exchange and valve testing. Power was returned to 100 percent on June 3, 2017. On June 5, 2017, power was reduced to 70 percent for a control rod sequence exchange. Power was returned to 100 percent on June 5, 2017. The unit remained at or near 100 percent RTP for the remainder of the inspection period.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection

a. Inspection Scope

Seasonal Extreme Weather Conditions

The inspectors conducted a detailed review of the stations adverse weather procedures written for extreme high temperatures. The inspectors verified that weather-related equipment deficiencies identified during the previous year had been placed into the work control process and/or corrected before the onset of seasonal extremes. The inspectors evaluated the licensees implementation of adverse weather preparation procedures and compensatory measures before the onset of seasonal extreme weather conditions.

Documents reviewed are listed in the Attachment.

The inspectors evaluated the following risk-significant systems:

  • transformer yard

b. Findings

No findings were identified.

==1R04 Equipment Alignment

a. Inspection Scope

Partial Walkdown (71111.04 - 4 samples)

==

The inspectors verified that critical portions of the selected systems were correctly aligned by performing partial walkdowns. The inspectors selected systems for assessment because they were a redundant or backup system or train, were important for mitigating risk for the current plant conditions, had been recently realigned, or were a single-train system. The inspectors determined the correct system lineup by reviewing plant procedures and drawings. Documents reviewed are listed in the Attachment.

The inspectors selected the following systems or trains to inspect:

  • Unit 2, CS train B

b. Findings

No findings were identified.

==1R05 Fire Protection

a. Inspection Scope

Quarterly Inspection (71111.05Q - 5 samples)

==

The inspectors evaluated the adequacy of selected pre-fire plans by comparing the pre-fire plans to the defined hazards and defense-in-depth features specified in the fire protection program. In evaluating the pre-fire plans, the inspectors assessed the following items:

  • control of transient combustibles and ignition sources
  • fire detection systems
  • water-based fire suppression systems
  • gaseous fire suppression systems
  • manual firefighting equipment and capability
  • passive fire protection features
  • compensatory measures and fire watches
  • issues related to fire protection contained in the licensees CAP

The inspectors toured the following fire areas to assess material condition and operational status of fire protection equipment. Documents reviewed are listed in the

.

  • 2PFP-TB2-01A, Unit 2 Turbine Building Breezeway, North 20 foot elevation
  • 1PFP-DG-05/04, Unit 1 Diesel Generator Cells 1-2, 23 foot elevation
  • 2PFP-TB2-01M, Unit 2 Turbine Building Laydown Area, 70 foot elevation
  • 2PFP-RB2-01T, Unit 2 Reactor Building Torus, 0 foot elevation

b. Findings

No findings were identified.

1R06 Flood Protection Measures

a. Inspection Scope

Underground Cables

The inspectors reviewed related flood analysis documents and inspected the areas listed below containing cables whose failure could disable risk-significant equipment. The inspectors directly observed the condition of cables and cable support structures and, as applicable, verified that dewatering devices and drainage systems were functioning properly. In addition, the inspectors verified the licensee was identifying and properly addressing issues using the CAP. Documents reviewed are listed in the Attachment.

  • Unit 2, manhole 2-MH-6NW, 2-MH-6SW

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification Program and Licensed Operator Performance

a. Inspection Scope

.1 Resident Inspector Quarterly Review of Licensed Operator Requalification

On June 1, 2017 the inspectors observed an evaluated simulator scenario, involving a NSW header leak and RCIC steam line break with failure to isolate, administered to an operating crew as part of the annual requalification operating test required by 10 CFR 55.59, Requalification.

The inspectors assessed the following:

  • licensed operator performance
  • the ability of the licensee to administer the scenario and evaluate the operators
  • the quality of the post-scenario critique
  • simulator performance

Documents reviewed are listed in the Attachment.

.2 Resident Inspector Quarterly Review of Licensed Operator Performance in the Actual

Plant/Main Control Room

The inspectors observed licensed operator performance in the main control room on April 14, 2017, during plant startup from Unit 2 refueling outage B223R1.

The inspectors assessed the following:

  • use of plant procedures
  • control board manipulations
  • communications between crew members
  • use and interpretation of instruments, indications, and alarms
  • use of human error prevention techniques
  • documentation of activities
  • management and supervision

Documents reviewed are listed in the Attachment.

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors assessed the licensees treatment of the issues listed below to verify the licensee appropriately addressed equipment problems within the scope of the maintenance rule (10 CFR 50.65, Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants). The inspectors reviewed procedures and records to evaluate the licensees identification, assessment, and characterization of the problems as well as their corrective actions for returning the equipment to a satisfactory condition. Documents reviewed are listed in the Attachment.

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed the maintenance activities listed below to verify that the licensee assessed and managed plant risk as required by 10 CFR 50.65(a)(4) and licensee procedures. The inspectors assessed the adequacy of the licensees risk assessments and implementation of risk management actions. The inspectors also verified that the licensee was identifying and resolving problems with assessing and managing maintenance-related risk using the CAP. Additionally, for maintenance resulting from unforeseen situations, the inspectors assessed the effectiveness of the licensees planning and control of emergent work activities. Documents reviewed are listed in the Attachment.

  • Unit 2, April 3, 2017, elevated risk during refueling outage B223R1 fuel movement
  • Unit 2, April 6, 2017, elevated risk during refueling outage B223R1 electrical work window
  • Unit 2, April 10, 2017, elevated risk during refueling outage B223R1 vessel draindown
  • Unit 2, May 15, 2017, elevated risk with 2-CAC-V17, reactor building to torus vacuum breaker, unplanned inoperability

b. Findings

No findings were identified.

1R15 Operability Determinations and Functionality Assessments

a. Inspection Scope

Operability and Functionality Review

The inspectors selected the operability determinations or functionality evaluations listed below for review based on the risk-significance of the associated components and systems. The inspectors reviewed the technical adequacy of the determinations to ensure that TS operability was properly justified and the components or systems remained capable of performing their design functions. To verify whether components or systems were operable, the inspectors compared the operability and design criteria in the appropriate sections of the TS and updated final safety analysis report to the licensees evaluations. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. Additionally, the inspectors reviewed a sample of corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with operability evaluations. Documents reviewed are listed in the Attachment.

  • Unit 2, RCIC high moisture content in turbine oil, NCR 2126899
  • Unit 2, RCIC steam leak, NCR 2127691

b. Findings

One licensee-identified violation was documented in Section 4OA7.

1R18 Plant Modifications

a. Inspection Scope

The inspectors verified that the plant modifications listed below did not affect the safety functions of important safety systems. The inspectors confirmed the modifications did not degrade the design bases, licensing bases, and performance capability of risk significant SSCs. The inspectors also verified modifications performed during plant configurations involving increased risk did not place the plant in an unsafe condition.

Additionally, the inspectors evaluated whether system operability and availability, configuration control, post-installation test activities, and changes to documents, such as drawings, procedures, and operator training materials, complied with licensee standards and NRC requirements. In addition, the inspectors reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with modifications. Documents reviewed are listed in the

.

  • NCR 2124497, Carabiners installed for barring gear locking pins on EDGs 1, 2 and 3
  • EC408181, Unit 2 RHR F047B, heat exchanger 2B inlet valve, motor replacement

b. Findings

No findings were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors either observed post-maintenance testing or reviewed the test results for the maintenance activities listed below to verify the work performed was completed correctly and the test activities were adequate to verify system operability and functional capability.

  • WO 20157390, Unit 2, RHR F047B, heat exchanger 2B inlet valve, motor replacement, May 30, 2017

The inspectors evaluated these activities for the following:

  • Acceptance criteria were clear and demonstrated operational readiness
  • Effects of testing on the plant were adequately addressed
  • Test instrumentation was appropriate
  • Tests were performed in accordance with approved procedures
  • Equipment was returned to its operational status following testing
  • Test documentation was properly evaluated

Additionally, the inspectors reviewed a sample of corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with post-maintenance testing. Documents reviewed are listed in the Attachment.

b. Findings

No findings were identified.

1R20 Refueling and Other Outage Activities

a. Inspection Scope

.1 Unit 2 Refueling Outage B223R1

Unit 2 began the inspection period in refueling outage B223R1. The inspectors reviewed outage plans and contingency plans for the Unit 2 refueling outage, which ended with the generator synchronization to the grid on April 15, 2017, to confirm that the licensee had appropriately considered risk, industry experience, and previous site-specific problems in developing and implementing a plan that assured maintenance of defense-in-depth of key safety functions.

During the refueling outage, the inspectors monitored licensee controls over the following outage activities:

  • Licensee configuration management, including maintenance of defense-in-depth for key safety functions and compliance with the applicable Technical Specifications (TSs) when taking equipment out of service
  • Implementation of clearance activities and confirmation that tags were properly hung and equipment appropriately configured to safely support the work or testing
  • Installation and configuration of reactor coolant pressure, level, and temperature instruments to provide accurate indication, accounting for instrument error
  • Controls over the status and configuration of electrical systems to ensure that TS and outage safety plan requirements were met, and controls over switchyard activities
  • Controls to ensure that outage work was not impacting the ability of the operators to operate the spent fuel pool cooling system
  • Reactor water inventory controls including flow paths, configurations, and alternative means for inventory addition, and controls to prevent inventory loss
  • Controls over activities that could affect reactivity
  • Startup and ascension to full power operation, tracking of startup prerequisites, walkdown of the drywell (primary containment) to verify that debris had not been left which could block emergency core cooling system suction strainers, and reactor physics testing
  • Licensee identification and resolution of problems related to refueling outage activities

Documents reviewed are listed in the Attachment.

.2 Unit 1 Maintenance Outage B120F1

For the Unit 1 maintenance outage to replace the 1B recirculation pump seal, from April 25, 2017, through April 28, 2017, the inspectors evaluated the following outage activities:

  • shutdown, cooldown, heatup, and startup
  • reactivity and inventory control
  • decay heat removal and spent fuel pool cooling system operation The inspectors verified that the licensee:
  • controlled plant configuration in accordance with administrative risk reduction methodologies
  • developed work schedules to manage fatigue
  • developed mitigation strategies for loss of key safety functions
  • adhered to operating license and TS requirements

Inspectors verified that safety-related and risk-significant SSCs not accessible during power operations were maintained in an operable condition. The inspectors also reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with outage activities. Documents reviewed are listed in the Attachment.

b. Findings

No findings were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors reviewed the surveillance tests listed below and either observed the test or reviewed test results to verify testing activities adequately demonstrated that the affected SSCs remained capable of performing the intended safety functions (under conditions as close as practical to design bases conditions or as required by TS) and maintained their operational readiness.

The inspectors evaluated the test activities to assess for preconditioning of equipment, procedure adherence, and equipment alignment following completion of the surveillance.

Additionally, the inspectors reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with surveillance testing. Documents reviewed are listed in the Attachment.

Routine Surveillance Tests

  • Procedure 2MST-RPS41R, RPS Logic System Functional Test, April 6, 2017

In-Service Tests (IST)

  • Procedure 0PT-09.2, HPCI System Operability Test, May 10, 2017

Reactor Coolant System Leak Detection

  • Procedure 0OI-02.3, Unit 1 Drywell Leakage Control, April 25, 2017

b. Findings

No findings were identified.

Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation

a. Inspection Scope

The inspectors observed the emergency preparedness drill conducted on June 1, 2017, involving a NSW header leak and RCIC steam line break with failure to isolate. The inspectors observed licensee activities in the simulator and technical support center to evaluate implementation of the emergency plan, including event classification, notification, and protective action recommendations. The inspectors evaluated the licensees performance against criteria established in the licensees procedures.

Additionally, the inspectors attended the post-exercise critique to assess the licensees effectiveness in identifying emergency preparedness weaknesses and verified the identified weaknesses were entered in the CAP. Documents reviewed are listed in the

.

b. Findings

No findings were identified.

OTHER ACTIVITIES

4OA1 Performance Indicator (PI) Verification

a. Inspection Scope

The inspectors reviewed a sample of the performance indicator data, submitted by the licensee, for the Unit 1 and Unit 2 PIs listed below. The inspectors reviewed plant records compiled between April 1, 2016, through March 31, 2017, to verify the accuracy and completeness of the data reported for the station. The inspectors verified that the PI data complied with guidance contained in Nuclear Energy Institute 99-02, Regulatory Assessment Performance Indicator Guideline, and licensee procedures. The inspectors verified the accuracy of reported data that were used to calculate the value of each PI.

In addition, the inspectors reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with PI data. Documents reviewed are listed in the Attachment.

Cornerstone: Mitigating Systems

  • Units 1 and 2, safety system functional failures
  • Units 1 and 2, emergency AC power system
  • Units 1 and 2, cooling water system

b. Findings

No findings were identified.

4OA2 Problem Identification and Resolution

.1 Routine Review

The inspectors screened items entered into the licensees corrective action program to identify repetitive equipment failures or specific human performance issues for follow-up.

The inspectors reviewed condition reports, attended screening meetings, or accessed the licensees computerized corrective action database.

.2 Semi-Annual Trend Review

a. Inspection Scope

The inspectors reviewed issues entered in the licensees corrective action program and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors focused their review on human performance trends during Unit 2 refueling outage B223R1, but also considered the results of inspector daily condition report screenings, licensee trending efforts, and licensee human performance results. The review nominally considered the 6-month period of January 1, 2017, through June 30, 2017, although some examples extended beyond those dates when the scope of the trend warranted. The inspectors compared their results with the licensees analysis of trends. Additionally, the inspectors reviewed the adequacy of corrective actions associated with a sample of the issues identified in the licensees trend reports. The inspectors also reviewed corrective action documents that were processed by the licensee to identify potential adverse trends in the condition of structures, systems, and/or components as evidenced by acceptance of long-standing non-conforming or degraded conditions. Documents reviewed are listed in the

.

b. Findings

No findings were identified.

.3 Annual Follow-Up of Selected Issues

a. Inspection Scope

The inspectors conducted a detailed review of the following condition report:

  • NCR 2120423, rising trend in Unit 2 suppression pool temperature, April 30, 2017

The inspectors evaluated the following attributes of the licensees actions:

  • complete and accurate identification of the problem in a timely manner
  • evaluation and disposition of operability and reportability issues
  • consideration of extent of condition, generic implications, common cause, and previous occurrences
  • classification and prioritization of the problem
  • identification of root and contributing causes of the problem
  • identification of any additional condition reports
  • completion of corrective actions in a timely manner

Documents reviewed are listed in the Attachment.

b. Findings

No findings were identified.

4OA3 Follow-up of Events

.1 (Closed) Licensee Event Report (LER) 05000324/2017-001-00, Implementation of

Enforcement Guidance Memorandum (EGM) 11-003, Revision 3

a. Inspection Scope

On March 22, 2017, Unit 2 implemented the guidance of EGM 11-003, Revision 3, Enforcement Guidance Memorandum on Dispositioning Boiling Water Reactor Licensee Noncompliance with TS Containment Requirements During Operations with a Potential for Draining the Reactor Vessel. Consistent with this EGM, secondary containment operability was not maintained during operations with the potential for draining the reactor vessel activities. The EGM guidance was implemented from March 22, 2017, at 1209 to March 28, 2017, at 1230. The activities are discussed in Section 4OA5.

Inspectors verified compliance with the guidelines of EGM 11-003 prior to and during these activities. The licensee has submitted a license amendment request to adopt TS Task Force traveler associated with generic resolution of this issue. The licensee entered this issue into the CAP as NCR 2110409. Documents reviewed are listed in the

.

b. Findings

The enforcement actions associated with this LER are documented in Sections 4OA5.

No findings were identified during the review of this LER. This LER is closed.

.2 (Closed) LER 05000324/2017-002-00, Plant Mode Change with Primary Containment

Inoperable

a. Inspection Scope

On April 13, 2017, Unit 2 was in Mode 4 preparing to exit refueling outage B223R1. The primary containment was being vented to ensure habitability during maintenance in the drywell. At 2347, the reactor was taken to Mode 2 with the primary containment still aligned for venting. In this condition, the drywell ventilation makes the primary containment inoperable due to the drywell and the suppression chamber being in communication to each other. With primary containment inoperable during startup, the plant violated Limiting Condition for Operation (LCO) 3.0.4, which requires all LCOs to be met for the plant condition prior to entry into the applicable mode.

The licensee reported this event in accordance with 10 CFR 50.72(b)(3)(v)(D), a non-emergency 8-hour report. The licensee also reported this event in accordance with 10 CFR 50.73(a)(2)(i)(B), for entering a condition prohibited by TSs, and 10 CFR 50.73(a)(2)(v)(D), for a loss of safety function. The cause of the event was the failure of operations personnel to initiate a tracking LCO for primary containment being inoperable in accordance with licensee procedure 0OI-01.01, BNP Conduct of Operations Supplement. The licensee determined a tracking LCO should have been initiated to ensure the primary containment was restored to operable prior to entering Mode 2. As immediate corrective actions, the licensee restored containment to operable on April 14, 2017, at 0030, and the Shift Manager and Control Room Supervisor were removed from shift. Further, a remediation plan was developed and implemented to assess the Shift Manager and Control Room Supervisor for watch standing and reinstatement. The licensee entered this issue into CAP as NCR 2116753. Documents reviewed are listed in the Attachment.

b. Findings

The enforcement actions associated with this LER are documented in Section 4OA7.

No findings were identified during the review of this LER. This LER is closed.

.3 (Closed) LER 05000325;324/2016-006-01, Control Room AC Units Inoperable Due to

Corroded Supports

a. Inspection Scope

On December 14, 2016, the 2D control room AC unit was declared inoperable due to corrosion on the support channels, and Units 1 and 2 entered TS 3.7.4, Condition A. On January 30, 2017, the 1D control room AC unit was declared inoperable for corrosion on the support channels. The corrosion was due to trapped moisture in contact with steel supports exposed to a local marine environment. The corrosion degraded the supports to the point that the safety function of the AC unit would be lost during a seismic event.

Since the degradation was due to corrosion, both units were determined to be inoperable at the same time. The conditions were determined to have existed longer than the TS 3.7.4 allowed outage time. The licensee entered this issue into the CAP as NCRs 2113799 and 2113800. As corrective actions, the licensee replaced both AC units supports, declared the units operable, and inspected the 2E control room AC unit for corrosion.

b. Findings

The inspectors identified the licensee failed to recognize the 1D AC unit was inoperable on December 1, 2016, during the periodic inspection. The inspectors documented an NRC-identified Green NCV in Inspection Report 05000325;324/2017001, Section 4OA2.

No additional findings were identified during the review of this LER. This LER is closed.

.4 (Closed) LER 05000325;324/2017-002, Foreign Material in Switch Results in Unplanned

Automatic Start of Emergency Diesel Generators

a. Inspection Scope

On April 17, 2017, Unit 2 was in Mode 1 at approximately 22 percent of rated power and was starting up from a refueling outage. Operators manually tripped the Unit 2 main turbine to halt increasing bearing vibration. The power circuit breakers for the Unit 2 main generator did not open as expected on the turbine trip, but subsequently opened when main generator reverse power relays actuated. This resulted in the automatic start of all four EDGs. The EDGs did not tie to emergency busses because offsite power was still available. This event was caused by a turbine stop valve limit switch failing to open due to foreign material intrusion. There was no safety impact of the failed limit switch.

The licensee entered this issue into the CAP as NCR 2117033. As corrective actions, the licensee will inspect similar switches during the next scheduled refueling outage on each unit (i.e., spring 2018 for Unit 1 and spring 2019 for Unit 2).

b. Findings

No findings were identified.

4OA5 Other Activities

.1 Implementation of EGM 11-003, Revision 3, Enforcement Guidance Memorandum on

Dispositioning Boiling Water Reactor Licensee Noncompliance with Technical Specification Containment Requirements During Operations with a Potential for Draining the Reactor Vessel

a. Inspection Scope

The inspectors reviewed the plants implementation of NRC EGM 11-003, Revision 3, during Unit 2 maintenance activities for operations with a potential for draining the reactor vessel (OPDRVs), during the Unit 2 refueling outage. Inspectors verified that for all dates, all other TS requirements were met during OPDRVs with secondary containment inoperable. Documents reviewed are listed in the Attachment.

b. Findings

Description.

During the Unit 2 refueling outage, the OPDRVs activities are listed below:

  • March 21, 2017: 6 gallons per minute leakage for maintenance associated with the 2B recirculation pump seal rebuild
  • March 23, 2017: 48 gallons per minute leakage for hydraulic control unit draining to support rod maintenance
  • March 27, 2017: 71.2 gallons per minute leakage to replace the low power range monitors and intermediate power range monitors

These activities took place without secondary containment being operable.

Enforcement.

TS 3.6.4.1, Secondary Containment, requires that secondary containment be operable and is applicable during OPDRVs. The required action if secondary containment is inoperable in this condition is to initiate actions to suspend OPDRVs immediately. Contrary to the above, on March 21, 2017, March 23, 2017, March 24, 2017, and March 27, 2017, the licensee failed to maintain secondary containment operable while performing OPDRVs.

However, because the violations were identified during the discretion period described in EGM 11-003, Revision 3, and the licensee met the criteria established in the EGM prior to and during these activities, the NRC exercised enforcement discretion (Enforcement Action-17-123) for the dates of March 21, 2017, March 23, 2017, March 24, 2017, and March 27, 2017, in accordance with Section 3.5, Violations Involving Special Circumstances, of the NRC Enforcement Policy and, therefore, will not issue enforcement action for this violation. The inspectors observed that Brunswick has already submitted a license amendment request (BSEP 17-0060) on June 29, 2017 which was accepted for review by the NRC on July 18, 2017. The licensee entered this issue into the CAP as NCR 2110409.

4OA6 Meetings, Including Exit

On July 12, 2017, the resident inspectors presented the inspection results to Mr. Gideon and other members of the licensees staff. The inspectors verified that no proprietary information was retained by the inspectors or documented in this report.

4OA7 Licensee Identified Violations

The following violation of very low safety significance (Green) was identified by the licensee and is a violation of NRC requirements which meet the criteria of the NRC Enforcement Policy, for being dispositioned as a non-cited violation.

  • LCO 3.0.4 states, in part, when an LCO is not met, entry into a MODE or other specified condition in the applicability shall only be made when the associated ACTIONS to be entered permit continued operation in the MODE for an unlimited period of time.

Contrary to the above, on April 13, 2017, at 2347, the licensee changed modes on Unit 2 from Mode 4 to Mode 2 with the primary containment inoperable. Specifically, TS 3.6.1.1, Primary Containment, requires primary containment to be operable in Modes 1, 2, and 3, however, the reactor was taken to Mode 2 with the primary containment still aligned for venting. In this condition, the drywell ventilation makes the primary containment inoperable due to the drywell and the suppression chamber being in communication to each other. This condition is allowed for two hours before the required action to shutdown to Mode 4 is required. Since the required action is not permitted for continued operation, a violation of LCO 3.0.4 occurred. The cause of the event was the failure of operations personnel to initiate a tracking LCO for primary containment being inoperable in accordance with licensee procedure 0OI-01.01, BNP Conduct of Operations Supplement. The licensee determined a tracking LCO should have been initiated to ensure the primary containment was restored to operable prior to entering Mode 2. As immediate corrective actions, the licensee restored containment to operable on April 14, 2017, at 0030, and the Shift Manager and Control Room Supervisor were removed from shift. Further, a remediation plan was developed and implemented to assess the Shift Manager and Control Room Supervisor for watch standing and reinstatement.

This finding is associated with the Barrier Integrity Cornerstone. Using IMC 0609, Appendix G, Shutdown Operations Significance Determination Process, 1, Exhibit 4, Barrier Integrity Screening Questions, the finding screened to Green because it did not degrade the ability to close or isolate the containment, it did not degrade the physical integrity of reactor containment, and it did not involve an actual reduction in function of hydrogen control. This issue was documented in the licensees CAP as NCR 2116753.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

K. Allen

Director, Design Engineering

B. Bagwell

Environmental & Chemistry

A. Baker

Supervisor, Environmental & Chemistry

J. Berry

Supervisor, LOCT Training

A. Brittain

Director, Nuclear Plant Security

P. Brown

Manager, Nuclear Performance Improvement

B. Bryant

Manager, Nuclear Oversight

J. Bryant

Regulatory Affairs

R. Carpenter

Radiation Monitor Engineer

P. Dubrouillet

Director, Nuclear Engineering, Mechanical Systems

C. Dunsmore

Manager, Nuclear Outage

W. Gideon

Vice President

L. Grzeck

Manager, Nuclear Regulatory Affairs

J. Hicks

Manager, Nuclear Training

B. Houston

Manager, Nuclear Maintenance

J. Johnson

Manager, Nuclear Chemistry

K. Krueger

Manager, Nuclear Operations

J. McAdoo

Manager, Nuclear Rad Protection

K. Moser

B. Murray

Plant Manager

Licensing

J. Nolin

General Manager, Nuclear Engineering

W. Orlando

Superintendent, E/I&C

O. Paladiy

Welding Engineer/Repair & Replacement Engineer

A. Padleckas

Assistant Ops Manager, Training

D. Petrusic

Superintendent, Environmental & Chemistry

J. Pierce

Manager, Nuclear Work Management

E. Rau

Operations Training

M. Regan

Project Manager, Major Projects

L. Rohrbaugh

Operator Training

M. Smiley

Manager, Nuclear Ops Training

L. Spencer

Operator Training

R. Wiemann

Director, Nuclear Engineering, Electrical Reactor Systems

E. Williams

Operations Manager

S. Williams

BWRVIP Program Engineer

C. Winslow

ISI Program Engineer

B. Wonton

Director, Nuclear Organizational Effectiveness

State of North Carolina

P. Cox

Department of Health and Human Services

NRC Personnel

S. Rose

Chief, Reactor Projects Branch 4

P. Niebaum

Acting Chief, Reactor Projects Branch 4

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000324/2017-001-00

LER

Implementation of Enforcement Guidance Memorandum (EGM) 11-003, Revision 3 (Section 4OA3.1)

05000324/2017-002-00 LER Plant Mode Change with Primary Containment Inoperable (Section 4OA3.2)
05000325;324/2016-006-01

LER

Control Room AC Units Inoperable Due to Corroded Supports (Section 4OA3.3)

05000325;324/2017-002 LER

Foreign Material in Switch Results in Unplanned Automatic Start of Emergency Diesel Generators (Section 4OA3.4)

LIST OF DOCUMENTS REVIEWED