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| issue date = 04/30/1987
| issue date = 04/30/1987
| title = Responds to Violations Noted in Insp Rept 50-311/87-03. Corrective Actions:Injection Capability to All Four Cold Legs Restored,Directive Issued Containing IE Info Notice 87-001 for Review & Procedure Sp (0) 4.5.3.1 Changed
| title = Responds to Violations Noted in Insp Rept 50-311/87-03. Corrective Actions:Injection Capability to All Four Cold Legs Restored,Directive Issued Containing IE Info Notice 87-001 for Review & Procedure Sp (0) 4.5.3.1 Changed
| author name = MCNEILL C A
| author name = Mcneill C
| author affiliation = PUBLIC SERVICE ELECTRIC & GAS CO. OF NEW JERSEY
| author affiliation = PUBLIC SERVICE ELECTRIC & GAS CO. OF NEW JERSEY
| addressee name =  
| addressee name =  
Line 14: Line 14:
| page count = 3
| page count = 3
}}
}}
See also: [[followed by::IR 05000311/1987003]]


=Text=
=Text=
{{#Wiki_filter:Public Service Electric and Gas Company ..... Corbin A. McNeil!, Jr. SeniorVice  
{{#Wiki_filter:Public Service Electric and Gas Company Corbin A. McNeil!, Jr.
President  
SeniorVice President -
-Nuclear Public Service Electric and Gas Company P.O. Box236, Hancocks Bridge, NJ 08038 609 339-4800 MR 3 o 1987 NLR-N87077  
Nuclear Public Service Electric and Gas Company P.O. Box236, Hancocks Bridge, NJ 08038 609 339-4800 MR 3 o 1987 NLR-N87077 United States Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 RESPONSE TO NOTICE OF VIOLATION NRC INSPECTION REPORT NO. 50-311/87-03 SALEM GENRATING STATION UNIT NO. 2 DOCKET NO. 50-311 Public Service Electric and Gas Company (PSE&G) has received the Notice of Violation dated March 31, 1987 regarding the inoperability of both Emergency Core Cooling System (ECCS)
United States Nuclear Regulatory  
Residual Heat Removal (RHR) subsystems for approximately twenty hours.
Commission  
Pursuant to the requirements of 10 CFR 2.201, our response to this Notice of Violation is provided in the attachment to this letter.
Document Control Desk Washington, DC 20555 RESPONSE TO NOTICE OF VIOLATION  
Attachment C
NRC INSPECTION  
Mr. D. C. Fischer Licensing Project Manager Mr. T. J. Kenny Senior Resident Inspector Sincerely, Mr. w. T. Russell, Administrator Region I  
REPORT NO. 50-311/87-03  
~~~5070009 870430 G
SALEM GENRATING  
ADOCK 05000311 PDR  
STATION UNIT NO. 2 DOCKET NO. 50-311 Public Service Electric and Gas Company (PSE&G) has received the Notice of Violation  
. -... -.. *-*-*--....... ~ ***-.  
dated March 31, 1987 regarding  
 
the inoperability  
'i  
of both Emergency  
*~-
Core Cooling System (ECCS) Residual Heat Removal (RHR) subsystems  
ATTACHMENT PUBLIC SERVICE ELECTRIC AND GAS COMPANY SALEM GENERATING STATION UNIT NO. 2 RESPONSE TO NOTICE OF VIOLATION Technical Specification Limiting Condition for Operation (LCO) 3.5.2 requires that while the reactor is in power operation, startup, or hot standby., two independent Emergency Core Cooling System (ECCS) subsystems shall be operable with each subsystem comprised, in part, of an operable Residual Heat Removal (RHR) pump and an operable flow path for low pressure safety injection.
for approximately  
The Final Safety Analysis Report Chapter 15 Accident Analysis for the large break loss of coolant accident was based on each RHR pump being capable of delivering low pressure safety injection flow to all four Reactor Coolant System (RCS) cold legs.
twenty hours. Pursuant to the requirements  
Technical Specification 3.0.3 requires that, when a Technical Specification LCO is not met, action shall be taken within one hour to place the unit in a mode in which the specification does not apply by placing it in hot ~tandby within the next 6 hours, hot shutdown within the following 6 hours, and cold shutdown within the subsequent 24 hours.
of 10 CFR 2.201, our response to this Notice of Violation  
Contrary to this, for approximately 20 hours on January 12 and 13,- 1987, neither of the ECCS subsystems met the conditions of LCO 3.5.2 in that only two of the required f iow cold injection paths were operable.
is provided in the attachment  
The subsystems were inoperable in that the injection valve (22 SJ 49) for one RHR pump as well as the RHR loop cross-tie valve (22 RH 19) were closed.
to this letter. Attachment  
These were closed in support of a pl~nned maintenance activity.
C Mr. D. C. Fischer Licensing  
This condition was identified by station personnel upon reviews performed pursuant to IE Information Notice 87-01.
Project Manager Mr. T. J. Kenny Senior Resident Inspector  
Technical Specification 3.0.3 was entered and the maintenance activity was terminated with the system returned to operable status.  
Sincerely, Mr. w. T. Russell, Administrator  
 
Region I  
===RESPONSE===
870430 G ADOCK 05000311 PDR . ---. -... -.. *-*-*--....... ***-. .*.*:.::*
PSE&G DOES NOT DISPUTE THE VIOLATION.
*.* 
T_he root cause of this violation is the fact that the Technical Specifications and the Updated Final Safety Analysis Report (UFSAR) do not clearly delineate the fact that injection into all four RCS cold legs is required to mee~ the design bases.
'i ATTACHMENT
Furthermore, a failure on the part of Westinghouse to promptly communicate previous industry occurrences of RHR misalignments precluded a more timely identification of this condition *at Salem Station.
PUBLIC SERVICE ELECTRIC AND GAS COMPANY SALEM GENERATING  
CORRECTIVE ACTIONS TAKEN AND RESULTS ACHIEVED The immediate corrective action taken by Salem Station personnel upon review of IE Information Notice 87-01, entitled "RHR Valve  
STATION UNIT NO. 2 RESPONSE TO NOTICE OF VIOLATION  
*Misalignment Causes Degradation of ECCS in PWRs," was to  
Technical  
 
Specification  
-,,;:.*-I'". '  
Limiting Condition  
'\\
for Operation (LCO) 3.5.2 requires that while the reactor is in power operation, startup, or hot standby., two independent  
. *.,~
Emergency  
'"\\,  
Core Cooling System (ECCS) subsystems  
~
shall be operable with each subsystem  
commence a unit shutdown.
comprised, in part, of an operable Residual Heat Removal (RHR) pump and an operable flow path for low pressure safety injection.  
Injection capability to all four cold legs was restored within three and a half hours after identification by station personnel.
The Final Safety Analysis Report Chapter 15 Accident Analysis for the large break loss of coolant accident was based on each RHR pump being capable of delivering  
Tpis action brought us into full compliance with Technical Specification 3.5.2.
low pressure safety injection  
An Operations Department Information Directive was issued to all Licensed Operators which contained a copy of IE Information Notice 87-01 for their review.
flow to all four Reactor Coolant System (RCS) cold legs. Technical  
Also included was an interpretation of Technical Specifications 3.5.2.e and 3.5.3.d.
Specification  
The interpretation defined what is required for an operable flow path of the RHR system, i.e., the capability to inject into all four RCS cold legs.
3.0.3 requires that, when a Technical  
In addition, the following actions were taken.
Specification  
First, Surveillance Procedure SP (0) 4.5.3.l was changed to reflect the requirement that both RH 19 valves and SJ 49 valves must be opened prior to changing from cold shutdown to hot shutdown.
LCO is not met, action shall be taken within one hour to place the unit in a mode in which the specification  
Second, included in the Second Ten-Year Inspection Inservice Testing Program submitted for NRC review on March 30, 1987,. is a request for relief from the ASME Section XI code requirement to perform a full stroke test of the SJ 49 and RH 19 valves on a quarterly basis.
does not apply by placing it in hot  
Currently, Technical Specification 3.0.3 is entered to perform this test.
within the next 6 hours, hot shutdown within the following  
Third, the Nuclear Training Department has incorporated into Segment 4 of the Licensed Operator Requalification training, a section on the design basis assumptions for ECCS equipment.
6 hours, and cold shutdown within the subsequent  
This training will be completed by June 30, 1987.
24 hours. Contrary to this, for approximately  
Fourth, a Technical Specification change request is being formulated which will clearly reflect the ECCS design bases requirements in Technical Specifications 3.5.2 and 3.5.3.
20 hours on January 12 and 13,-1987, neither of the ECCS subsystems  
Finally, UFSAR changes have been processed that explicitly identify the ECCS design bases requirements for injection capability into all four RCS cold legs.
met the conditions  
These changes will be issued in Amendment No. 7 to the Salem Station UFSAR.
of LCO 3.5.2 in that only two of the required f iow cold injection  
* These actions help to ensure that the ECCS design basis requirements are met and maintained, and will serve to preclude a similar occurrence.
paths were operable.  
The following actions have been taken to improve the communication process between PSE&G And Westinghouse Electric Corporation.
The subsystems  
PSE&G has contacted Westinghouse upper level management on two separate occasions tp strongly express concern over their failure to provide prompt notification of similar problems that occtirred at the Byron and Trojan Nuclear Plants.
were inoperable  
Westinghouse was reminded of the importance of timely operating experience feedback and.their obligation to their customers.
in that the injection  
In  
valve (22 SJ 49) for one RHR pump as well as the RHR loop * cross-tie  
. their response, Westinghouse indicated that, while they consider this to be an isolated case, they.have taken steps to improve their customer notification process.
valve (22 RH 19) were closed. These were closed in support of a  
The PSE&GNuclear Department's Industry Operating Experience Evaluation Program assures that applicable industry experiences are evaluated for any potential impact on Salem or Hope Creek Generating Stations *. The program is dependent on industry feedback.
maintenance  
This program, together with the reaffirmation of Westinghouse's obligations to its customers, provides adequate assurance of the timely dissemination of industry concerns and should serve to preclude reoccurrence of this event.}}
activity.  
This condition  
was identified  
by station personnel  
upon reviews performed  
pursuant to IE Information  
Notice 87-01. Technical  
Specification  
3.0.3 was entered and the maintenance  
activity was terminated  
with the system returned to operable status. RESPONSE PSE&G DOES NOT DISPUTE THE VIOLATION.  
T_he root cause of this violation  
is the fact that the Technical  
Specifications  
and the Updated Final Safety Analysis Report (UFSAR) do not clearly delineate  
the fact that injection  
into all four RCS cold legs is required to  
the design bases. Furthermore, a failure on the part of Westinghouse  
to promptly communicate  
previous industry occurrences  
of RHR misalignments  
precluded  
a more timely identification  
of this condition  
*at Salem Station. CORRECTIVE  
ACTIONS TAKEN AND RESULTS ACHIEVED The immediate  
corrective  
action taken by Salem Station personnel  
upon review of IE Information  
Notice 87-01, entitled "RHR Valve *Misalignment  
Causes Degradation  
of ECCS in PWRs," was to
. , .. * ... -, ---,,;:.*-I'" . ' '\ . *. '"\, * commence a unit shutdown.  
Injection  
capability  
to all four cold legs was restored within three and a half hours after identification  
by station personnel.  
Tpis action brought us into full compliance  
with Technical  
Specification  
3.5.2. An Operations  
Department  
Information  
Directive  
was issued to all Licensed Operators  
which contained  
a copy of IE Information  
Notice 87-01 for their review. Also included was an interpretation  
of Technical  
Specifications  
3.5.2.e and 3.5.3.d. The interpretation  
defined what is required for an operable flow path of the RHR system, i.e., the capability  
to inject into all four RCS cold legs. In addition, the following  
actions were taken. First, Surveillance  
Procedure  
SP (0) 4.5.3.l was changed to reflect the requirement  
that both RH 19 valves and SJ 49 valves must be opened prior to changing from cold shutdown to hot shutdown.  
Second, included in the Second Ten-Year Inspection  
Inservice  
Testing Program submitted  
for NRC review on March 30, 1987, . is a request for relief from the ASME Section XI code requirement  
to perform a full stroke test of the SJ 49 and RH 19 valves on a quarterly  
basis. Currently, Technical  
Specification  
3.0.3 is entered to perform this test. Third, the Nuclear Training Department  
has incorporated  
into Segment 4 of the Licensed Operator Requalification  
training, a section on the design basis assumptions  
for ECCS equipment.  
This training will be completed  
by June 30, 1987. Fourth, a Technical  
Specification  
change request is being formulated  
which will clearly reflect the ECCS design bases requirements  
in Technical  
Specifications  
3.5.2 and 3.5.3. Finally, UFSAR changes have been processed  
that explicitly  
identify the ECCS design bases requirements  
for injection  
capability  
into all four RCS cold legs. These changes will be issued in Amendment  
No. 7 to the Salem Station UFSAR. * These actions help to ensure that the ECCS design basis requirements  
are met and maintained, and will serve to preclude a similar occurrence.  
The following  
actions have been taken to improve the communication  
process between PSE&G And Westinghouse  
Electric Corporation.  
PSE&G has contacted  
Westinghouse  
upper level management  
on two separate occasions  
tp strongly express concern over their failure to provide prompt notification  
of similar problems that occtirred  
at the Byron and Trojan Nuclear Plants. Westinghouse  
was reminded of the importance  
of timely operating  
experience  
feedback and.their  
obligation  
to their customers.  
In . their response, Westinghouse  
indicated  
that, while they consider this to be an isolated case, they.have  
taken steps to improve their customer notification
process. The PSE&GNuclear  
Department's  
Industry Operating  
Experience  
Evaluation  
Program assures that applicable  
industry experiences  
are evaluated  
for any potential  
impact on Salem or Hope Creek Generating  
Stations *. The program is dependent  
on industry feedback.  
This program, together with the reaffirmation  
of Westinghouse's  
obligations  
to its customers, provides adequate assurance  
of the timely dissemination  
of industry concerns and should serve to preclude reoccurrence  
of this event.
}}

Latest revision as of 04:12, 6 January 2025

Responds to Violations Noted in Insp Rept 50-311/87-03. Corrective Actions:Injection Capability to All Four Cold Legs Restored,Directive Issued Containing IE Info Notice 87-001 for Review & Procedure Sp (0) 4.5.3.1 Changed
ML18092B552
Person / Time
Site: Salem PSEG icon.png
Issue date: 04/30/1987
From: Corbin McNeil
Public Service Enterprise Group
To:
NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM)
References
IEIN-87-001, IEIN-87-1, NLR-N87077, NUDOCS 8705070009
Download: ML18092B552 (3)


Text

Public Service Electric and Gas Company Corbin A. McNeil!, Jr.

SeniorVice President -

Nuclear Public Service Electric and Gas Company P.O. Box236, Hancocks Bridge, NJ 08038 609 339-4800 MR 3 o 1987 NLR-N87077 United States Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 RESPONSE TO NOTICE OF VIOLATION NRC INSPECTION REPORT NO. 50-311/87-03 SALEM GENRATING STATION UNIT NO. 2 DOCKET NO. 50-311 Public Service Electric and Gas Company (PSE&G) has received the Notice of Violation dated March 31, 1987 regarding the inoperability of both Emergency Core Cooling System (ECCS)

Residual Heat Removal (RHR) subsystems for approximately twenty hours.

Pursuant to the requirements of 10 CFR 2.201, our response to this Notice of Violation is provided in the attachment to this letter.

Attachment C

Mr. D. C. Fischer Licensing Project Manager Mr. T. J. Kenny Senior Resident Inspector Sincerely, Mr. w. T. Russell, Administrator Region I

~~~5070009 870430 G

ADOCK 05000311 PDR

. -... -.. *-*-*--....... ~ ***-.

'i

  • ~-

ATTACHMENT PUBLIC SERVICE ELECTRIC AND GAS COMPANY SALEM GENERATING STATION UNIT NO. 2 RESPONSE TO NOTICE OF VIOLATION Technical Specification Limiting Condition for Operation (LCO) 3.5.2 requires that while the reactor is in power operation, startup, or hot standby., two independent Emergency Core Cooling System (ECCS) subsystems shall be operable with each subsystem comprised, in part, of an operable Residual Heat Removal (RHR) pump and an operable flow path for low pressure safety injection.

The Final Safety Analysis Report Chapter 15 Accident Analysis for the large break loss of coolant accident was based on each RHR pump being capable of delivering low pressure safety injection flow to all four Reactor Coolant System (RCS) cold legs.

Technical Specification 3.0.3 requires that, when a Technical Specification LCO is not met, action shall be taken within one hour to place the unit in a mode in which the specification does not apply by placing it in hot ~tandby within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />, hot shutdown within the following 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />, and cold shutdown within the subsequent 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

Contrary to this, for approximately 20 hours2.314815e-4 days <br />0.00556 hours <br />3.306878e-5 weeks <br />7.61e-6 months <br /> on January 12 and 13,- 1987, neither of the ECCS subsystems met the conditions of LCO 3.5.2 in that only two of the required f iow cold injection paths were operable.

The subsystems were inoperable in that the injection valve (22 SJ 49) for one RHR pump as well as the RHR loop cross-tie valve (22 RH 19) were closed.

These were closed in support of a pl~nned maintenance activity.

This condition was identified by station personnel upon reviews performed pursuant to IE Information Notice 87-01.

Technical Specification 3.0.3 was entered and the maintenance activity was terminated with the system returned to operable status.

RESPONSE

PSE&G DOES NOT DISPUTE THE VIOLATION.

T_he root cause of this violation is the fact that the Technical Specifications and the Updated Final Safety Analysis Report (UFSAR) do not clearly delineate the fact that injection into all four RCS cold legs is required to mee~ the design bases.

Furthermore, a failure on the part of Westinghouse to promptly communicate previous industry occurrences of RHR misalignments precluded a more timely identification of this condition *at Salem Station.

CORRECTIVE ACTIONS TAKEN AND RESULTS ACHIEVED The immediate corrective action taken by Salem Station personnel upon review of IE Information Notice 87-01, entitled "RHR Valve

  • Misalignment Causes Degradation of ECCS in PWRs," was to

-,,;:.*-I'". '

'\\

. *.,~

'"\\,

~

commence a unit shutdown.

Injection capability to all four cold legs was restored within three and a half hours after identification by station personnel.

Tpis action brought us into full compliance with Technical Specification 3.5.2.

An Operations Department Information Directive was issued to all Licensed Operators which contained a copy of IE Information Notice 87-01 for their review.

Also included was an interpretation of Technical Specifications 3.5.2.e and 3.5.3.d.

The interpretation defined what is required for an operable flow path of the RHR system, i.e., the capability to inject into all four RCS cold legs.

In addition, the following actions were taken.

First, Surveillance Procedure SP (0) 4.5.3.l was changed to reflect the requirement that both RH 19 valves and SJ 49 valves must be opened prior to changing from cold shutdown to hot shutdown.

Second, included in the Second Ten-Year Inspection Inservice Testing Program submitted for NRC review on March 30, 1987,. is a request for relief from the ASME Section XI code requirement to perform a full stroke test of the SJ 49 and RH 19 valves on a quarterly basis.

Currently, Technical Specification 3.0.3 is entered to perform this test.

Third, the Nuclear Training Department has incorporated into Segment 4 of the Licensed Operator Requalification training, a section on the design basis assumptions for ECCS equipment.

This training will be completed by June 30, 1987.

Fourth, a Technical Specification change request is being formulated which will clearly reflect the ECCS design bases requirements in Technical Specifications 3.5.2 and 3.5.3.

Finally, UFSAR changes have been processed that explicitly identify the ECCS design bases requirements for injection capability into all four RCS cold legs.

These changes will be issued in Amendment No. 7 to the Salem Station UFSAR.

  • These actions help to ensure that the ECCS design basis requirements are met and maintained, and will serve to preclude a similar occurrence.

The following actions have been taken to improve the communication process between PSE&G And Westinghouse Electric Corporation.

PSE&G has contacted Westinghouse upper level management on two separate occasions tp strongly express concern over their failure to provide prompt notification of similar problems that occtirred at the Byron and Trojan Nuclear Plants.

Westinghouse was reminded of the importance of timely operating experience feedback and.their obligation to their customers.

In

. their response, Westinghouse indicated that, while they consider this to be an isolated case, they.have taken steps to improve their customer notification process.

The PSE&GNuclear Department's Industry Operating Experience Evaluation Program assures that applicable industry experiences are evaluated for any potential impact on Salem or Hope Creek Generating Stations *. The program is dependent on industry feedback.

This program, together with the reaffirmation of Westinghouse's obligations to its customers, provides adequate assurance of the timely dissemination of industry concerns and should serve to preclude reoccurrence of this event.