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=Text=
=Text=
{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION ber 30, 2018
{{#Wiki_filter:October 30, 2018


==SUBJECT:==
==SUBJECT:==
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Sincerely,
Sincerely,
/RA/
/RA/  
Matthew Young, Chief Reactor Projects Branch 6 Division of Reactor Projects Docket Numbers: 50-334 and 50-412 License Numbers: DPR-66 and NPF-73
 
Matthew Young, Chief Reactor Projects Branch 6 Division of Reactor Projects  
 
Docket Numbers: 50-334 and 50-412 License Numbers: DPR-66 and NPF-73  


===Enclosure:===
===Enclosure:===
Inspection Report 05000334/2018003 and 05000412/2018003
Inspection Report 05000334/2018003 and 05000412/2018003  


==Inspection Report==
==Inspection Report==
Docket Numbers: 50-334 and 50-412 License Numbers: DPR-66 and NPF-73 Report Numbers: 05000334/2018003 and 05000412/2018003 Enterprise Identifier: I-2018-003-0073 Licensee: FirstEnergy Nuclear Operating Company (FENOC)
Docket Numbers:
Facility: Beaver Valley Power Station, Units 1 and 2 Location: Shippingport, PA 15077 Inspection Dates: July 1, 2018 to September 30, 2018 Inspectors: J. Krafty, Senior Resident Inspector S. Horvitz, Resident Inspector R. Rolph, Health Physicist K. Mangan, Senior Reactor Inspector P. Ott, Operations Engineer L. Dumont, Reactor Inspector A. Turilin, Reactor Inspector N. Floyd, Senior Reactor Inspector Approved By: M. Young, Chief Reactor Projects Branch 6 Division of Reactor Projects Enclosure
50-334 and 50-412  
 
License Numbers:
DPR-66 and NPF-73  
 
Report Numbers:
05000334/2018003 and 05000412/2018003  
 
Enterprise Identifier: I-2018-003-0073  
 
Licensee:
FirstEnergy Nuclear Operating Company (FENOC)  
 
Facility:
Beaver Valley Power Station, Units 1 and 2  
 
Location:
Shippingport, PA 15077  
 
Inspection Dates:
July 1, 2018 to September 30, 2018  
 
Inspectors:
J. Krafty, Senior Resident Inspector  
 
S. Horvitz, Resident Inspector  
 
R. Rolph, Health Physicist  
 
K. Mangan, Senior Reactor Inspector  
 
P. Ott, Operations Engineer  
 
L. Dumont, Reactor Inspector  
 
A. Turilin, Reactor Inspector  
 
N. Floyd, Senior Reactor Inspector  
 
Approved By:
M. Young, Chief  
 
Reactor Projects Branch 6  
 
Division of Reactor Projects  


=SUMMARY=
=SUMMARY=
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring FirstEnergy Nuclear
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring FirstEnergy Nuclear  


Operating Companys (FENOCs) performance at Beaver Valley Power Station Units 1 and 2 by conducting the baseline inspections described in this report in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. NRC identified and self-revealed findings, violations, and additional items are summarized in the table below.
Operating Companys (FENOCs) performance at Beaver Valley Power Station Units 1 and 2 by conducting the baseline inspections described in this report in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. NRC identified and self-revealed findings, violations, and additional items are summarized in the table below.


List of Findings and Violations Inadequate Verification of Full Low Head Safety Injection Suction Piping Cornerstone           Significance                             Cross-Cutting       Report Aspect              Section Mitigating           Green                                     [H.11] - Human 71111.15 Systems              NCV 05000334/2018003-01                  Performance -
===List of Findings and Violations===
Closed                                    Challenge the Unknown A self-revealed Green non-cited violation (NCV) of technical specification (TS) 5.4.1,
Inadequate Verification of Full Low Head Safety Injection Suction Piping Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000334/2018003-01 Closed
[H.11] - Human Performance -
Challenge the Unknown 71111.15 A self-revealed Green non-cited violation (NCV) of technical specification (TS) 5.4.1,
Procedures, was identified when FENOC failed to adequately implement procedure 1OM-52.4.R.2.A, Station Startup Mode 6 to Mode 1 Administrative and Local Actions, to verify that the low head safety injection (LHSI) suction pipes were full of water. Specifically, the non-destructive examination (NDE) inspector incorrectly determined that the suction pipes were full which led to inoperability of one or more trains of LHSI for in excess of four hours on May 22, 2018, when the suction lines were found to be voided.
Procedures, was identified when FENOC failed to adequately implement procedure 1OM-52.4.R.2.A, Station Startup Mode 6 to Mode 1 Administrative and Local Actions, to verify that the low head safety injection (LHSI) suction pipes were full of water. Specifically, the non-destructive examination (NDE) inspector incorrectly determined that the suction pipes were full which led to inoperability of one or more trains of LHSI for in excess of four hours on May 22, 2018, when the suction lines were found to be voided.


=PLANT STATUS=
=PLANT STATUS=


===Unit 1 began the inspection period at 48 percent power due to a tube leak in the condenser.
Unit 1 began the inspection period at 48 percent power due to a tube leak in the condenser.


The unit was returned to rated thermal power on July 3, 2018, and remained at or near rated thermal power for the remainder of the inspection period.
The unit was returned to rated thermal power on July 3, 2018, and remained at or near rated thermal power for the remainder of the inspection period.
Line 67: Line 116:


==REACTOR SAFETY==
==REACTOR SAFETY==
==71111.01 - Adverse Weather Protection==
==71111.01 - Adverse Weather Protection==
 
===External Flooding (1 Sample)===
===External Flooding===
{{IP sample|IP=IP 71111.01|count=1}}
 
The inspectors evaluated readiness to cope with external flooding during the week of August 27, 2018.
The inspectors evaluated readiness to cope with external flooding during the week of August 27, 2018.


==71111.04 - Equipment Alignment==
==71111.04 - Equipment Alignment==
 
===Partial Walkdown (3 Samples)===
===Partial Walkdown===
{{IP sample|IP=IP 71111.04|count=3}}
 
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
: (1) Unit 1, river water system following post maintenance testing of the A river water pump on July 13, 2018
: (1) Unit 1, river water system following post maintenance testing of the A river water pump on July 13, 2018
Line 86: Line 128:


==71111.05A/Q - Fire Protection Annual/Quarterly==
==71111.05A/Q - Fire Protection Annual/Quarterly==
 
===Quarterly Inspection (5 Samples)===
===Quarterly Inspection===
{{IP sample|IP=IP 71111.05A/Q|count=5}}
 
The inspectors evaluated fire protection program implementation in the following selected areas:
The inspectors evaluated fire protection program implementation in the following selected areas:
: (1) Unit 1, auxiliary feedwater and quench spray pumps, fire compartment 2-SB-2 on July 9, 2018
: (1) Unit 1, auxiliary feedwater and quench spray pumps, fire compartment 2-SB-2 on July 9, 2018
Line 98: Line 137:


==71111.11 - Licensed Operator Requalification Program and Licensed Operator Performance==
==71111.11 - Licensed Operator Requalification Program and Licensed Operator Performance==
 
===Operator Requalification (1 Sample)===
===Operator Requalification===
{{IP sample|IP=IP 71111.11|count=1}}
 
The inspectors observed and evaluated a crew of licensed operators in the Unit 2 simulator during the annual licensed operator requalification exam on July 31, 2018.
The inspectors observed and evaluated a crew of licensed operators in the Unit 2 simulator during the annual licensed operator requalification exam on July 31, 2018.


Operator Requalification Examination Results (Annual) (1 Sample)===
===Operator Requalification Examination Results (Annual) (1 Sample)===
The inspectors reviewed and evaluated the Unit 1 requalification written examination
The inspectors reviewed and evaluated the Unit 1 requalification written examination (operating test results reviewed in first quarter report) results on September 5, 2018.
 
===(operating test results reviewed in first quarter report) results on September 5, 2018.


The inspectors reviewed and evaluated the Unit 2 requalification examination (operating test) results on September 5, 2018.
The inspectors reviewed and evaluated the Unit 2 requalification examination (operating test) results on September 5, 2018.


Operator Performance (1 Sample)===
===Operator Performance (1 Sample)===
The inspectors observed power ascension following waterbox repairs at Unit 1 on July 3, 2018,
The inspectors observed power ascension following waterbox repairs at Unit 1 on July 3, 2018, and A feedwater heater train repairs at Unit 2 on July 24, 2018.
 
===and A feedwater heater train repairs at Unit 2 on July 24, 2018.


==71111.12 - Maintenance Effectiveness==
==71111.12 - Maintenance Effectiveness==
 
===Routine Maintenance Effectiveness (1 Sample)===
===Routine Maintenance Effectiveness===
{{IP sample|IP=IP 71111.12|count=1}}
 
The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:
The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:
: (1) Emergency response facility diesel generator failure on July 6, 2018
: (1) Emergency response facility diesel generator failure on July 6, 2018


==71111.13 - Maintenance Risk Assessments and Emergent Work Control==
==71111.13 - Maintenance Risk Assessments and Emergent Work Control==
 
{{IP sample|IP=IP 71111.13|count=5}}
==={{IP sample|IP=IP 71111.13|count=5}}


The inspectors evaluated the risk assessments for the following planned and emergent work activities:
The inspectors evaluated the risk assessments for the following planned and emergent work activities:
Line 162: Line 190:


==71111.22 - Surveillance Testing==
==71111.22 - Surveillance Testing==
The inspectors evaluated the following surveillance tests:


The inspectors evaluated the following surveillance tests:
===Routine===
Routine===
{{IP sample|IP=IP 71111.22|count=3}}
{{IP sample|IP=IP 71111.13|count=3}}
: (1) 1OST-7.18C, Safety Injection Relay Test (Slave Relay K609) - Train A on July 12, 2018
: (1) 1OST-7.18C, Safety Injection Relay Test (Slave Relay K609) - Train A on July 12, 2018
: (2) 1OST-24.2, Motor Driven Auxiliary Feed Pump Test [1FW-P-3A] on July 16, 2018
: (2) 1OST-24.2, Motor Driven Auxiliary Feed Pump Test [1FW-P-3A] on July 16, 2018
Line 171: Line 199:


==71114.06 - Drill Evaluation==
==71114.06 - Drill Evaluation==
 
===Drill/Training Evolution (1 Sample)===
===Drill/Training Evolution===
The inspectors evaluated a simulator training evolution for Unit 2 licensed operators on July 31,
{{IP sample|IP=IP 71114.06|count=1}}
 
The inspectors evaluated a simulator training evolution for Unit 2 licensed operators on July 31, 2018.


==RADIATION SAFETY==
==RADIATION SAFETY==
==71124.05 - Radiation Monitoring Instrumentation==
==71124.05 - Radiation Monitoring Instrumentation==
 
===Walk Downs and Observations (1 Sample)===
===Walk Downs and Observations===
{{IP sample|IP=IP 71124.05|count=1}}
 
The inspectors evaluated radiation monitoring instrumentation during plant walkdowns.
The inspectors evaluated radiation monitoring instrumentation during plant walkdowns.


Calibration and Testing Program (1 Sample)===
===Calibration and Testing Program (1 Sample)===
The inspectors evaluated the licensees calibration and testing program.
The inspectors evaluated the licensees calibration and testing program.


=====OTHER ACTIVITIES - BASELINE==
==OTHER ACTIVITIES - BASELINE==
===71151 - Performance Indicator Verification


===71151 - Performance Indicator Verification The inspectors verified licensee performance indicator submittals listed below for the period from July 1, 2017, through June 30, 2018 ===
The inspectors verified licensee performance indicator submittals listed below for the period from July 1, 2017, through June 30, 2018===
{{IP sample|IP=IP 71151|count=6}}
{{IP sample|IP=IP 71151|count=6}}
: (1) Unit 1 and 2, Heat Removal System
: (1) Unit 1 and 2, Heat Removal System
Line 198: Line 220:


==71152 - Problem Identification and Resolution==
==71152 - Problem Identification and Resolution==
 
===Semiannual Trend Review (1 Sample)===
===Semiannual Trend Review===
{{IP sample|IP=IP 71152|count=1}}
 
The inspectors reviewed the licensees corrective action program for trends that might be indicative of a more significant safety issue.
The inspectors reviewed the licensees corrective action program for trends that might be indicative of a more significant safety issue.


Annual Follow-up of Selected Issues (2 Samples)===
===Annual Follow-up of Selected Issues (2 Samples)===
The inspectors reviewed the licensees implementation of its corrective action program
The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:
 
===related to the following issues:
: (1) Condition Report 2017-11593, Full Inspection of Unit-1 Iso-phase Bus Duct Not Completed
: (1) Condition Report 2017-11593, Full Inspection of Unit-1 Iso-phase Bus Duct Not Completed
: (2) Condition Report 2017-03937, Severity Level IV Violation for Failure to Obtain Prior NRC Authorization.
: (2) Condition Report 2017-03937, Severity Level IV Violation for Failure to Obtain Prior NRC Authorization.


===71153 - Follow-up of Events and Notices of Enforcement Discretion Personnel Performance ===
===71153 - Follow-up of Events and Notices of Enforcement Discretion Personnel Performance===
{{IP sample|IP=IP 71153|count=2}}
{{IP sample|IP=IP 71153|count=2}}
The inspectors evaluated response during the following non-routine evolutions or transients.
The inspectors evaluated response during the following non-routine evolutions or transients.
: (1) Unit 2 unplanned power reduction to 40 percent due to a feedwater heater level control valve failure causing instability in the feedwater heater system on July 20, 2018.
: (1) Unit 2 unplanned power reduction to 40 percent due to a feedwater heater level control valve failure causing instability in the feedwater heater system on July 20, 2018.
: (2) Unit 2 TS required shutdown due to the loss of a 480 volt emergency bus on August 12, 2018.
: (2) Unit 2 TS required shutdown due to the loss of a 480 volt emergency bus on August 12, 2018.


Notice of Enforcement Discretion (1 Sample)===
===Notice of Enforcement Discretion (1 Sample)===
The inspectors evaluated FENOCs actions surrounding Notice of Enforcement Discretion No. 18-1-01 which can be accessed at http://www.nrc.gov/reading-rm/doc-collections/enforcement/notices/noedreactor.html on August 13, 2018. The inspectors verified the accuracy of the Notice of Enforcement Discretion and its consistency with Beaver Valley Power Stations oral assertions and implementation of compensatory measures and commitments.
The inspectors evaluated FENOCs actions surrounding Notice of Enforcement Discretion No. 18-1-01 which can be accessed at http://www.nrc.gov/reading-rm/doc-collections/enforcement/notices/noedreactor.html on August 13, 2018. The inspectors verified the accuracy of the Notice of Enforcement Discretion and its consistency with Beaver Valley Power Stations oral assertions and implementation of compensatory measures and commitments.


==OTHER ACTIVITIES==
==OTHER ACTIVITIES==
- TEMPORARY INSTRUCTIONS, INFREQUENT, AND ABNORMAL Impact of Financial Conditions on Continued Safe Performance In that the licensee's parent company, FirstEnergy Solutions, was under bankruptcy protection/reorganization during the inspection period, NRC Region I conducted reviews of processes at Beaver Valley. Using the flexibilities in the baseline inspection program, the inspectors evaluated several aspects of FENOCs operations to assess whether any identified plant performance issues could be related to the station's financial condition. The factors reviewed included:
- TEMPORARY INSTRUCTIONS, INFREQUENT, AND ABNORMAL  
 
Impact of Financial Conditions on Continued Safe Performance  
 
In that the licensee's parent company, FirstEnergy Solutions, was under bankruptcy protection/reorganization during the inspection period, NRC Region I conducted reviews of processes at Beaver Valley. Using the flexibilities in the baseline inspection program, the inspectors evaluated several aspects of FENOCs operations to assess whether any identified plant performance issues could be related to the station's financial condition. The factors reviewed included:
: (1) impact on regulatory required plant staffing,
: (1) impact on regulatory required plant staffing,
: (2) corrective maintenance backlog,
: (2) corrective maintenance backlog,
Line 229: Line 251:


==INSPECTION RESULTS==
==INSPECTION RESULTS==
Inadequate Verification of Full Low Head Safety Injection Suction Piping Cornerstone             Significance                           Cross-Cutting       Report Aspect              Section Mitigating               Green                                   [H.11] - Human 71111.15 Systems                  NCV 05000334/2018003-01                Performance -
Inadequate Verification of Full Low Head Safety Injection Suction Piping Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000334/2018003-01 Closed
Closed                                  Challenge the Unknown A self-revealed Green non-cited violation (NCV) of technical specification (TS) 5.4.1, Procedures, was identified when FENOC failed to adequately implement procedure 1OM-52.4.R.2.A, Station Startup Mode 6 to Mode 1 Administrative and Local Actions, to verify that the low head safety injection (LHSI) suction pipes were full of water. Specifically, the non-destructive examination (NDE) inspector incorrectly determined that the suction pipes were full, which led to inoperability of one or more trains of LHSI for in excess of four hours on May 22, 2018, when the suction lines were found to be voided.
[H.11] - Human Performance - Challenge the Unknown 71111.15 A self-revealed Green non-cited violation (NCV) of technical specification (TS) 5.4.1, Procedures, was identified when FENOC failed to adequately implement procedure 1OM-52.4.R.2.A, Station Startup Mode 6 to Mode 1 Administrative and Local Actions, to verify that the low head safety injection (LHSI) suction pipes were full of water. Specifically, the non-destructive examination (NDE) inspector incorrectly determined that the suction pipes were full, which led to inoperability of one or more trains of LHSI for in excess of four hours on May 22, 2018, when the suction lines were found to be voided.


=====Description:=====
=====Description:=====
Line 243: Line 265:
Corrective Actions: FENOC took immediate corrective action to restore operability of the LHSI system and subsequently reassessed the voids and determined that the system would have remained operable.
Corrective Actions: FENOC took immediate corrective action to restore operability of the LHSI system and subsequently reassessed the voids and determined that the system would have remained operable.


Corrective Action Reference: CR 2018-04735
Corrective Action Reference: CR 2018-04735  


=====Performance Assessment:=====
=====Performance Assessment:=====
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Disposition: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.
Disposition: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.


Observations                                             71152 The inspectors noted that there were two over temperature delta temperature (OTDT)surveillance failures in the past two years. No individual component failed, but the cumulative tolerances of the individual components caused the loop to exceed the TS allowed values for OTDT delta temperature and OTDT average temperature. Additionally, there were four surveillances in the past three years where the results were close to the TS limit (greater than 75 percent of the allowed range). In one instance, a calibration was performed. In the three instances where a calibration was not performed, the channel failed the following surveillance twice. The inspectors noted that typical strategies used to minimize failures such as, a surveillance range which is smaller than the allowable TS limit range, an as-found band and a smaller as-left band, or trending of surveillance results and recommending corrective action when a negative trend develops, have not been implemented. FENOC documented this issue in CR-2018-08899.
Observations 71152 The inspectors noted that there were two over temperature delta temperature (OTDT)surveillance failures in the past two years. No individual component failed, but the cumulative tolerances of the individual components caused the loop to exceed the TS allowed values for OTDT delta temperature and OTDT average temperature. Additionally, there were four surveillances in the past three years where the results were close to the TS limit (greater than 75 percent of the allowed range). In one instance, a calibration was performed. In the three instances where a calibration was not performed, the channel failed the following surveillance twice. The inspectors noted that typical strategies used to minimize failures such as, a surveillance range which is smaller than the allowable TS limit range, an as-found band and a smaller as-left band, or trending of surveillance results and recommending corrective action when a negative trend develops, have not been implemented. FENOC documented this issue in CR-2018-08899.


Observations                                         71152 The inspectors reviewed the root cause analysis and the corrective actions taken to address the iso-phase bus short circuit which resulted in a reactor trip. The inspectors also reviewed the license renewal commitments submitted for the metal enclosed busses to mitigate degradation of the bus and enclosure. The inspectors concluded that the cause analysis was thorough, the extent of condition was sufficient to identify the scope of the problem, and the corrective actions addressed the deficiencies. The inspectors also determined that license renewal commitments related to metal enclosed bus inspections were met.
Observations 71152 The inspectors reviewed the root cause analysis and the corrective actions taken to address the iso-phase bus short circuit which resulted in a reactor trip. The inspectors also reviewed the license renewal commitments submitted for the metal enclosed busses to mitigate degradation of the bus and enclosure. The inspectors concluded that the cause analysis was thorough, the extent of condition was sufficient to identify the scope of the problem, and the corrective actions addressed the deficiencies. The inspectors also determined that license renewal commitments related to metal enclosed bus inspections were met.


Observations                                         71152 The inspectors performed an in-depth review of FENOCs corrective actions associated with CR-2017-03937 for the Severity Level IV Violation for failure to obtain prior NRC authorization before implementing an alternative to the American Society of Mechanical Engineers Operation and Maintenance Code requirements. The details of this violation were previously documented in NRC Inspection Report 05000334/2017001 (ADAMS Accession Number ML17135A162). The inspectors interviewed engineering staff and reviewed FENOCs maintenance and testing activities to further assess the cause and corrective actions. As a result of the issue, FENOC submitted a relief request to the NRC, which was subsequently approved in a letter dated March 2, 2017. FENOC staff tested the residual heat removal relief valve, RV-1RH-721, during the spring 2018 refueling outage with satisfactory results. FENOC also provided supplemental training on the issue and violation to engineering staff during a periodic training session. The inspectors determined FENOCs overall response to the issue was commensurate with the safety significance, was timely, and included appropriate corrective actions.
Observations 71152 The inspectors performed an in-depth review of FENOCs corrective actions associated with CR-2017-03937 for the Severity Level IV Violation for failure to obtain prior NRC authorization before implementing an alternative to the American Society of Mechanical Engineers Operation and Maintenance Code requirements. The details of this violation were previously documented in NRC Inspection Report 05000334/2017001 (ADAMS Accession Number ML17135A162). The inspectors interviewed engineering staff and reviewed FENOCs maintenance and testing activities to further assess the cause and corrective actions. As a result of the issue, FENOC submitted a relief request to the NRC, which was subsequently approved in a letter dated March 2, 2017. FENOC staff tested the residual heat removal relief valve, RV-1RH-721, during the spring 2018 refueling outage with satisfactory results. FENOC also provided supplemental training on the issue and violation to engineering staff during a periodic training session. The inspectors determined FENOCs overall response to the issue was commensurate with the safety significance, was timely, and included appropriate corrective actions.


==EXIT MEETINGS AND DEBRIEFS==
==EXIT MEETINGS AND DEBRIEFS==
Line 294: Line 316:
NOP-WM-2003, Work Management Surveillance Process, Revision 8
NOP-WM-2003, Work Management Surveillance Process, Revision 8
Condition Reports
Condition Reports
2001-0406                 2016-09904               2018-05926            2018-07931
2001-0406
2008-46771                2018-05678                2018-06101             2018-08493
2008-46771
2010-74947                2018-05700                2018-07441
2010-74947
2016-09904
2018-05678
2018-05700
2018-05926
2018-06101
2018-07441
2018-07931
2018-08493
Miscellaneous
Miscellaneous
2.029-0035, Low Head Safety Injection Pump Air Entrainment Analysis, December 2008
2.029-0035, Low Head Safety Injection Pump Air Entrainment Analysis, December 2008
601188892
601188892
Cause Analysis Report- Unexpected Gas Voids Between MOV-1SI-860A/B and the CNMT
Cause Analysis Report-Unexpected Gas Voids Between MOV-1SI-860A/B and the CNMT
Sump
Sump
EER 601171557, Eval Void Volume
EER 601171557, Eval Void Volume
Line 320: Line 350:
1/2-HPP-4.06.016, Mirion Alpha Beta Particulate Monitor - 203M, Revision 0
1/2-HPP-4.06.016, Mirion Alpha Beta Particulate Monitor - 203M, Revision 0
1-HPP-5.01.002, Emergency Operation of the PING Particulate, Iodine and Noble Gas
1-HPP-5.01.002, Emergency Operation of the PING Particulate, Iodine and Noble Gas
Monitors, Revision 5
Monitors, Revision 5  
 
2-HPP-5.04.001, Emergency Operation of the WRGM Assembly, Revision 3
2-HPP-5.04.001, Emergency Operation of the WRGM Assembly, Revision 3
NOP-OP-4401, Radiation Protection Instrumentation Program, Revision 3
NOP-OP-4401, Radiation Protection Instrumentation Program, Revision 3
Line 327: Line 358:
NOP-OP-4410, Fluke 451 B Calibration and Use, Revision 01
NOP-OP-4410, Fluke 451 B Calibration and Use, Revision 01
Work Order
Work Order
200607668                 200502462               200645197               200645313
200607668
200615254                  200596574                200536876               200578837
200615254
200667939                  200535882                200669339
200667939
200634673                  200698514                200552455
200634673
200370216                  200597266                200632692
200370216
200502462
200596574
200535882
200698514
200597266
200645197
200536876
200669339
200552455
200632692
200645313
200578837
71152
71152
Procedures
Procedures
NOP-LP-2001, Corrective Action Program, Revision 45
NOP-LP-2001, Corrective Action Program, Revision 45
Condition Reports
Condition Reports
2016-12335                 2017-11215              2018-04593              2018-06893
2016-12335
2017-05664                2017-11238               2018-04783               2018-08232
2017-05664
2017-11134                2018-02783              2018-05678
2017-11134
2017-11215
2017-11238
2018-02783
2018-04593
2018-04783
2018-05678
2018-06893
2018-08232
Work Orders
Work Orders
200121564                 200209770               200469979               200734302
200121564
200121594                  200429521                200643913
200121594
200209770
200429521
200469979
200643913
200734302
Miscellaneous
Miscellaneous
1/2-ADM-2306, Metal Enclosed Bus Program, Rev. 0
1/2-ADM-2306, Metal Enclosed Bus Program, Rev. 0

Latest revision as of 09:56, 5 January 2025

Integrated Inspection Report 05000334/2018003 and 05000412/2018003
ML18306A463
Person / Time
Site: Beaver Valley
Issue date: 10/30/2018
From: Matt Young
NRC/RGN-I/DRP/PB6
To: Bologna R
FirstEnergy Nuclear Operating Co
References
IR 2018003
Download: ML18306A463 (15)


Text

October 30, 2018

SUBJECT:

BEAVER VALLEY POWER STATION, UNIT NOS. 1 AND 2 - INTEGRATED INSPECTION REPORT 05000334/2018003 AND 05000412/2018003

Dear Mr. Bologna:

On September 30, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Beaver Valley Power Station, Units 1 and 2. On October 11, 2018, the NRC inspectors discussed the results of this inspection with Rodney Penfield, General Plant Manager and other members of your staff. The results of this inspection are documented in the enclosed report.

NRC inspectors documented one finding of very low safety significance (Green) in this report.

This finding involved a violation of NRC requirements. The NRC is treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2.a of the Enforcement Policy.

If you contest the violation or significance of the NCV, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement; and the NRC Resident Inspector at Beaver Valley Power Station. In addition, if you disagree with a cross-cutting aspect assignment or a finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U. S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC, 20555-0001; with copies to the Regional Administrator, Region I, and the NRC Resident Inspector at Beaver Valley Power Station. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations (10 CFR), Part 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Matthew Young, Chief Reactor Projects Branch 6 Division of Reactor Projects

Docket Numbers: 50-334 and 50-412 License Numbers: DPR-66 and NPF-73

Enclosure:

Inspection Report 05000334/2018003 and 05000412/2018003

Inspection Report

Docket Numbers:

50-334 and 50-412

License Numbers:

DPR-66 and NPF-73

Report Numbers:

05000334/2018003 and 05000412/2018003

Enterprise Identifier: I-2018-003-0073

Licensee:

FirstEnergy Nuclear Operating Company (FENOC)

Facility:

Beaver Valley Power Station, Units 1 and 2

Location:

Shippingport, PA 15077

Inspection Dates:

July 1, 2018 to September 30, 2018

Inspectors:

J. Krafty, Senior Resident Inspector

S. Horvitz, Resident Inspector

R. Rolph, Health Physicist

K. Mangan, Senior Reactor Inspector

P. Ott, Operations Engineer

L. Dumont, Reactor Inspector

A. Turilin, Reactor Inspector

N. Floyd, Senior Reactor Inspector

Approved By:

M. Young, Chief

Reactor Projects Branch 6

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring FirstEnergy Nuclear

Operating Companys (FENOCs) performance at Beaver Valley Power Station Units 1 and 2 by conducting the baseline inspections described in this report in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. NRC identified and self-revealed findings, violations, and additional items are summarized in the table below.

List of Findings and Violations

Inadequate Verification of Full Low Head Safety Injection Suction Piping Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000334/2018003-01 Closed

[H.11] - Human Performance -

Challenge the Unknown 71111.15 A self-revealed Green non-cited violation (NCV) of technical specification (TS) 5.4.1,

Procedures, was identified when FENOC failed to adequately implement procedure 1OM-52.4.R.2.A, Station Startup Mode 6 to Mode 1 Administrative and Local Actions, to verify that the low head safety injection (LHSI) suction pipes were full of water. Specifically, the non-destructive examination (NDE) inspector incorrectly determined that the suction pipes were full which led to inoperability of one or more trains of LHSI for in excess of four hours on May 22, 2018, when the suction lines were found to be voided.

PLANT STATUS

Unit 1 began the inspection period at 48 percent power due to a tube leak in the condenser.

The unit was returned to rated thermal power on July 3, 2018, and remained at or near rated thermal power for the remainder of the inspection period.

Unit 2 began the inspection period at rated thermal power. On July 20, 2018, the unit reduced power to 40 percent due to a feedwater heater level control valve failure causing instability in the feedwater heating system. The unit was returned to rated thermal power on July 24, 2018.

On August 12, 2018, the unit performed a TS required shutdown due to the loss of a 480 volt emergency bus. The unit was returned to rated thermal power on August 16, 2018, and remained at or near rated thermal power for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

External Flooding (1 Sample)

The inspectors evaluated readiness to cope with external flooding during the week of August 27, 2018.

71111.04 - Equipment Alignment

Partial Walkdown (3 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Unit 1, river water system following post maintenance testing of the A river water pump on July 13, 2018
(2) Unit 1, A train of auxiliary feedwater system following A motor driven auxiliary feedwater pump surveillance test on July 16, 2018
(3) Unit 2, A train of service water during C service water pump surveillance test on July 25, 2018

71111.05A/Q - Fire Protection Annual/Quarterly

Quarterly Inspection (5 Samples)

The inspectors evaluated fire protection program implementation in the following selected areas:

(1) Unit 1, auxiliary feedwater and quench spray pumps, fire compartment 2-SB-2 on July 9, 2018
(2) Unit 2, normal switchgear room, fire compartment 2-SB-4 on July 10, 2018
(3) Unit 1, main feedwater regulating valve room, ventilation equipment room, and clean shop, fire compartment 1-SB-GEN on July 17, 2018
(4) Unit 2, condensate polishing building, fire compartment 2-CP-1 on July 26, 2018
(5) Unit 2, alternate shutdown panel room, fire compartment 2-ASP on September 24, 2018

71111.11 - Licensed Operator Requalification Program and Licensed Operator Performance

Operator Requalification (1 Sample)

The inspectors observed and evaluated a crew of licensed operators in the Unit 2 simulator during the annual licensed operator requalification exam on July 31, 2018.

Operator Requalification Examination Results (Annual) (1 Sample)

The inspectors reviewed and evaluated the Unit 1 requalification written examination (operating test results reviewed in first quarter report) results on September 5, 2018.

The inspectors reviewed and evaluated the Unit 2 requalification examination (operating test) results on September 5, 2018.

Operator Performance (1 Sample)

The inspectors observed power ascension following waterbox repairs at Unit 1 on July 3, 2018, and A feedwater heater train repairs at Unit 2 on July 24, 2018.

71111.12 - Maintenance Effectiveness

Routine Maintenance Effectiveness (1 Sample)

The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:

(1) Emergency response facility diesel generator failure on July 6, 2018

71111.13 - Maintenance Risk Assessments and Emergent Work Control

The inspectors evaluated the risk assessments for the following planned and emergent work activities:

(1) Unit 2, elevated risk due to B charging pump and emergency response facility transformer maintenance on July 27, 2018
(2) Unit 2, elevated risk due to unavailability of 2-2 emergency diesel generator (EDG) on August 2, 2018
(3) Unit 2, unplanned immediate maintenance on the 2-2 and 2-4 batteries on August 12, 2018
(4) Unit 2, risk management and compensatory actions required to comply with the notice of enforcement discretion granted for restoration of the B train batteries following the loss of 2-9P 480 volt bus on August 13, 2018
(5) Unit 2, yellow risk due to loss of 2-9P 480 volt bus on August 13, 2018

71111.15 - Operability Determinations and Functionality Assessments

The inspectors evaluated the following operability determinations and functionality assessments:

(1) Unit 2, turbine driven auxiliary feedwater pump steamline isolation valve, 2MSS-SOV105B, stroke times on July 6, 2018
(2) Unit 1, over temperature delta temperature channel 432 exceeded the TS allowable value on July 30, 2018
(3) Unit 1, 1-2 EDG C fuel oil transfer pump, 1EE-P-1C, flow rate high out of acceptable range on August 22, 2018
(4) Unit 1, low head safety injection suction piping voiding on August 31, 2018
(5) Unit 2, 2-2 EDG output breaker, 2F10, failed to close on September 26, 2018

71111.18 - Plant Modifications

The inspectors evaluated the following temporary or permanent modifications:

(1) Engineering Change Package 14-0623-003, Temporary Modification to Secure Damper Vanes for 1VS-D-57B1 in the Open Position

71111.19 - Post Maintenance Testing

The inspectors evaluated post maintenance testing for the following maintenance/repair activities:

(1) Unit 2, turbine driven auxiliary feedwater pump steamline isolation valve, 2MSS-SOV105B, coil and reed switch replacement on July 9, 2018
(2) Unit 2, A charging pump planned maintenance on July 13, 2018
(3) Unit 2, replacement of airline components on FCV-1FW-479, bypass feedwater regulating valve on July 24, 2018
(4) Unit 1 & 2, emergency response facility diesel generator governor planned maintenance on July 31, 2018
(5) Unit 2, 2F11 relay replacement following loss of 2-9P bus on August 13, 2018

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Routine

(1) 1OST-7.18C, Safety Injection Relay Test (Slave Relay K609) - Train A on July 12, 2018
(2) 1OST-24.2, Motor Driven Auxiliary Feed Pump Test [1FW-P-3A] on July 16, 2018
(3) 1OST-36.22A, Diesel Generator 1-1 Simulated Undervoltage Start Signal on August 8, 2018

71114.06 - Drill Evaluation

Drill/Training Evolution (1 Sample)

The inspectors evaluated a simulator training evolution for Unit 2 licensed operators on July 31,

RADIATION SAFETY

71124.05 - Radiation Monitoring Instrumentation

Walk Downs and Observations (1 Sample)

The inspectors evaluated radiation monitoring instrumentation during plant walkdowns.

Calibration and Testing Program (1 Sample)

The inspectors evaluated the licensees calibration and testing program.

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification

The inspectors verified licensee performance indicator submittals listed below for the period from July 1, 2017, through June 30, 2018===

(1) Unit 1 and 2, Heat Removal System
(2) Unit 1 and 2, Residual Heat Removal Systems
(3) Unit 1 and 2, Cooling Water System

71152 - Problem Identification and Resolution

Semiannual Trend Review (1 Sample)

The inspectors reviewed the licensees corrective action program for trends that might be indicative of a more significant safety issue.

Annual Follow-up of Selected Issues (2 Samples)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) Condition Report 2017-11593, Full Inspection of Unit-1 Iso-phase Bus Duct Not Completed
(2) Condition Report 2017-03937, Severity Level IV Violation for Failure to Obtain Prior NRC Authorization.

71153 - Follow-up of Events and Notices of Enforcement Discretion Personnel Performance

The inspectors evaluated response during the following non-routine evolutions or transients.

(1) Unit 2 unplanned power reduction to 40 percent due to a feedwater heater level control valve failure causing instability in the feedwater heater system on July 20, 2018.
(2) Unit 2 TS required shutdown due to the loss of a 480 volt emergency bus on August 12, 2018.

Notice of Enforcement Discretion (1 Sample)

The inspectors evaluated FENOCs actions surrounding Notice of Enforcement Discretion No. 18-1-01 which can be accessed at http://www.nrc.gov/reading-rm/doc-collections/enforcement/notices/noedreactor.html on August 13, 2018. The inspectors verified the accuracy of the Notice of Enforcement Discretion and its consistency with Beaver Valley Power Stations oral assertions and implementation of compensatory measures and commitments.

OTHER ACTIVITIES

- TEMPORARY INSTRUCTIONS, INFREQUENT, AND ABNORMAL

Impact of Financial Conditions on Continued Safe Performance

In that the licensee's parent company, FirstEnergy Solutions, was under bankruptcy protection/reorganization during the inspection period, NRC Region I conducted reviews of processes at Beaver Valley. Using the flexibilities in the baseline inspection program, the inspectors evaluated several aspects of FENOCs operations to assess whether any identified plant performance issues could be related to the station's financial condition. The factors reviewed included:

(1) impact on regulatory required plant staffing,
(2) corrective maintenance backlog,
(3) changes to the planned maintenance schedule,
(4) corrective action program implementation, and
(5) reduction in outage scope, including risk-significant modifications. In particular, the inspectors assessed whether FENOC personnel continued to identify problems at an appropriate threshold and entered these problems into the corrective action program for resolution. The inspectors also assessed whether FENOC continued to develop and implement corrective actions commensurate with the safety significance of the problems identified.

INSPECTION RESULTS

Inadequate Verification of Full Low Head Safety Injection Suction Piping Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000334/2018003-01 Closed

[H.11] - Human Performance - Challenge the Unknown 71111.15 A self-revealed Green non-cited violation (NCV) of technical specification (TS) 5.4.1, Procedures, was identified when FENOC failed to adequately implement procedure 1OM-52.4.R.2.A, Station Startup Mode 6 to Mode 1 Administrative and Local Actions, to verify that the low head safety injection (LHSI) suction pipes were full of water. Specifically, the non-destructive examination (NDE) inspector incorrectly determined that the suction pipes were full, which led to inoperability of one or more trains of LHSI for in excess of four hours on May 22, 2018, when the suction lines were found to be voided.

Description:

On May 22, 2018, at 1256, Unit 1 personnel, while performing 3BVT01.11.04, Void Monitoring, discovered voids in the LHSI system between the containment sump and the suction isolation valves for both pumps. The voids were greater than 5 cubic feet, which exceeded the procedures acceptance criteria of 0.261 cubic feet. Both trains of LHSI were declared inoperable and TS 3.5.2, Condition C, and limiting condition for operation (LCO)3.0.3 were entered. The A train suction line was filled and LCO 3.0.3 was exited at 1559.

The B train suction line was then filled and TS 3.5.2 was exited at 1743.

FENOCs investigation concluded that, based on the amount of inventory that was lost, a total of 158 gallons, and interviews with the workers, the voids were most likely caused by water being pumped out as part of the containment sump inspection on May 5, 2018. Ultrasonic examination of the LHSI suction piping was performed on May 7, 2018, in accordance with FENOCs station startup procedure, 1OM-52.4.R.2.A, and documented that the LHSI suction lines were full. Interviews with the contract worker who performed the void monitoring indicated that although he was a qualified Level II NDE inspector, he primarily performed weld inspections and did not have significant experience inspecting piping for voids. He also mentioned experiencing difficulties performing the void monitoring procedure. FENOC concluded that the void monitoring results on May 7, 2018, were in error.

FENOC subsequently performed a reassessment of the voids found on May 22, 2018, and determined that during a design basis accident, the filing of the containment sump would have reduced the size of the voids and the LHSI pumps would have remained operable. The inspectors reviewed the calculations and agreed with the conclusion.

Corrective Actions: FENOC took immediate corrective action to restore operability of the LHSI system and subsequently reassessed the voids and determined that the system would have remained operable.

Corrective Action Reference: CR 2018-04735

Performance Assessment:

Performance Deficiency: The inspectors determined that FENOCs failure to adequately implement the station startup procedure, 1OM-52.4.R.2.A, as required by TS 5.4.1, was within their ability to foresee and prevent and therefore was a performance deficiency.

Specifically, FENOC failed to accurately determine the voids in the LHSI piping on May 7, 2018, which caused them to incorrectly enter Mode 4 without a satisfactory ultrasonic test of the LHSI suction lines.

Screening: The inspectors determined the performance deficiency was more than minor because it adversely affected the human performance attribute of the Mitigating Systems cornerstone and its objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.

Significance: The inspectors assessed the significance of the finding using IMC0609.04, Initial Characterization of Findings, and IMC 0609, Appendix A, Exhibit 2, Mitigating Systems Screening Questions. The inspectors determined that the finding did not represent a loss of system or function, did not result in the loss of a single train for greater that its TS allowed outage time, and did not result in an actual loss of function of one or more non-TS trains of equipment designated as high safety-significant for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

Therefore, the inspectors determined the finding to be of very low safety significance (Green).

Cross-Cutting Aspect: The finding has a cross cutting aspect in the area of Human Performance - Challenge the Unknown, because the individual performing the test did not stop when he had difficulties performing the void monitoring procedure.

Enforcement:

Violation: TS 5.4.1, Procedures, requires, in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Regulatory Guide (RG) 1.33, Revision 2, Appendix A, February 1978. RG 1.33, Appendix A recommended procedures include plant operating procedures for taking the plant from cold shutdown to hot standby. Procedure 1OM-52.4.R.2.A, Station Startup Mode 6 to Mode 1 Administrative and Local Actions, requires that satisfactory ultrasonic test (UT)examinations of the LHSI piping from the containment sump to the suction of the LHSI pumps have been completed prior to entering Mode 4.

Contrary to the above, on May 7, 2018, FENOC failed to properly perform UT examinations of the LHSI suction piping in accordance with 1OM-52.4.R.2.A prior to entering Mode 4.

Specifically, the NDE inspector incorrectly determined that the LHSI suction pipes were full which led to the inoperability of one or more trains of LHSI for greater than four hours on May 22, 2018, when the suction lines were found to be voided.

Disposition: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

Observations 71152 The inspectors noted that there were two over temperature delta temperature (OTDT)surveillance failures in the past two years. No individual component failed, but the cumulative tolerances of the individual components caused the loop to exceed the TS allowed values for OTDT delta temperature and OTDT average temperature. Additionally, there were four surveillances in the past three years where the results were close to the TS limit (greater than 75 percent of the allowed range). In one instance, a calibration was performed. In the three instances where a calibration was not performed, the channel failed the following surveillance twice. The inspectors noted that typical strategies used to minimize failures such as, a surveillance range which is smaller than the allowable TS limit range, an as-found band and a smaller as-left band, or trending of surveillance results and recommending corrective action when a negative trend develops, have not been implemented. FENOC documented this issue in CR-2018-08899.

Observations 71152 The inspectors reviewed the root cause analysis and the corrective actions taken to address the iso-phase bus short circuit which resulted in a reactor trip. The inspectors also reviewed the license renewal commitments submitted for the metal enclosed busses to mitigate degradation of the bus and enclosure. The inspectors concluded that the cause analysis was thorough, the extent of condition was sufficient to identify the scope of the problem, and the corrective actions addressed the deficiencies. The inspectors also determined that license renewal commitments related to metal enclosed bus inspections were met.

Observations 71152 The inspectors performed an in-depth review of FENOCs corrective actions associated with CR-2017-03937 for the Severity Level IV Violation for failure to obtain prior NRC authorization before implementing an alternative to the American Society of Mechanical Engineers Operation and Maintenance Code requirements. The details of this violation were previously documented in NRC Inspection Report 05000334/2017001 (ADAMS Accession Number ML17135A162). The inspectors interviewed engineering staff and reviewed FENOCs maintenance and testing activities to further assess the cause and corrective actions. As a result of the issue, FENOC submitted a relief request to the NRC, which was subsequently approved in a letter dated March 2, 2017. FENOC staff tested the residual heat removal relief valve, RV-1RH-721, during the spring 2018 refueling outage with satisfactory results. FENOC also provided supplemental training on the issue and violation to engineering staff during a periodic training session. The inspectors determined FENOCs overall response to the issue was commensurate with the safety significance, was timely, and included appropriate corrective actions.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On October 11, 2018, the inspectors presented the quarterly resident inspector inspection results to Mr. Rodney Penfield, General Plant Manager, and other members of the Beaver Valley Power Station staff.

DOCUMENTS REVIEWED

71111.13

Miscellaneous

Beaver Valley Unit 2 Week 7/23/2018, T-0 ICDP Profile, Revision 0

Beaver Valley Unit 2 Week 7/30/2018, T-0 ICDP Profile, Revision 0

Beaver Valley Unit 2 Week 08/06/2018, T-0 ICDP Profile, Revision 2

Narrative Logs 8/13/2018 Daylight

71111.15

Procedures

1MSP-13-RS Sump -1M, Containment Sump Inspection, Revision 6

1MSP-6.40-I, T-RC432 Delta T TAVG Protection Instrument Channel III Calibration, Revision 44

1MSP-6.79-I, Operational Alignment of Process Temperature Instrumentation, Revision 9

1OM-11.4.J, Filling and Venting the Safety Injection System, Revision 27

2OST-36.2, Emergency Diesel Generator [2EGS*EG2-2] Monthly Test, Revision 75

NOP-WM-2003, Work Management Surveillance Process, Revision 8

Condition Reports

2001-0406

2008-46771

2010-74947

2016-09904

2018-05678

2018-05700

2018-05926

2018-06101

2018-07441

2018-07931

2018-08493

Miscellaneous

2.029-0035, Low Head Safety Injection Pump Air Entrainment Analysis, December 2008

601188892

Cause Analysis Report-Unexpected Gas Voids Between MOV-1SI-860A/B and the CNMT

Sump

EER 601171557, Eval Void Volume

EER 601173192, Volume for BV1 LHSI Suction Piping

FAI/09-130, Technical Basis for Gas Transport to the Pump Suction, December 2009

MPR-3255, Beaver Valley Unit 1 Low Head Safety Injection Pump Past Operability Analysis,

Revision 2

NEI 09-10, Guidelines for Effective Prevention and Management of System Gas Accumulation,

Revision 1a-A

SP-1RC-19, Uncertainty Calculations for the 1.4% Uprated Conditions

WCAP-17276-P, Investigation of Simplified Equation for Gas Transport, Revision 1

71124.05

Procedures

1/2-HPP-4.06.007, Portable Air Sampler - Model HD-28 (RADECO), Revision 3

1/2-HPP-4.06.011, Portable Air Sampler - Model RAS-1 (Eberline Instruments), Revision 3

1/2-HPP-4.06.012, Eberline, AMS-4 Continuous Air Monitor, Revision 13

1/2-HPP-4.06.014, Gilian Air Sampler, Revision 1

1/2-HPP-4.06.015, Gilian Air Sampler Calibration, Revision 2

1/2-HPP-4.06.016, Mirion Alpha Beta Particulate Monitor - 203M, Revision 0

1-HPP-5.01.002, Emergency Operation of the PING Particulate, Iodine and Noble Gas

Monitors, Revision 5

2-HPP-5.04.001, Emergency Operation of the WRGM Assembly, Revision 3

NOP-OP-4401, Radiation Protection Instrumentation Program, Revision 3

NOP-OP-4404, PCM-2 Calibration, Source Checks and Use, Revision 4

NOP-OP-4408, Portable Survey Instruments, Revision 00

NOP-OP-4410, Fluke 451 B Calibration and Use, Revision 01

Work Order 200607668

200615254

200667939

200634673

200370216

200502462

200596574

200535882

200698514

200597266

200645197

200536876

200669339

200552455

200632692

200645313

200578837

71152

Procedures

NOP-LP-2001, Corrective Action Program, Revision 45

Condition Reports

2016-12335

2017-05664

2017-11134

2017-11215

2017-11238

2018-02783

2018-04593

2018-04783

2018-05678

2018-06893

2018-08232

Work Orders

200121564

200121594

200209770

200429521

200469979

200643913

200734302

Miscellaneous

1/2-ADM-2306, Metal Enclosed Bus Program, Rev. 0

1/2PMP-35-GML/TRF-03E, Iso-Phase Bus Inspection and Test, Issue 4 Rev. 6

1/2PMP-35-GML/TRF-03E, Iso-Phase Bus Inspection and Test, Issue 4 Rev. 7

DWG 08700-01.019, Shts. 1, 2, 3, and 4, Layout of Single Insulator Isolated Phase Bus Duct -

Main Transformer to Station Transformer, Revs. B, B, E, and F

FLOV-ES-BV-16-04, Fleet Oversight Escalation - Gaps in behaviors during plant activities,

Revision 0

FLOV-EL-BV-16-11, Fleet Oversight Elevation - Gaps in preventing foreign material from

entering plant systems and components, Revision 0

LER 2017-003-00, Beaver Valley Power Station Unit 1 Reactor Trip due to Turbine Trip and

Automatic Initiation of Auxiliary Feedwater System, Rev. 0

NOBP-ER-3015, License Renewal Implementation Guidelines, Rev. 01

PA-BV-2018-0002-007, Transient combustible walk down - Unit 1 Turbine Building

PA-BV-2018-0004-008, Deficiencies with documentation and record keeping

PA-BV-2018-0007-006, Environmental/chemical control in Unit 1 turbine building

PA-BV-2018-0008-001, Review of 1R25 Scope Change Request Deletions

PA-BV-2018-0008-004, Compliance with Appendix J Program Requirements for Not

Acceptable Test Results

L-16-317, Beaver Valley Unit 1 Letter - Proposed Alternative VRR5 to Delay Valve Test, dated

October 24, 2016