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=Text= | =Text= | ||
{{#Wiki_filter: | {{#Wiki_filter:November 7, 2019 | ||
==SUBJECT:== | ==SUBJECT:== | ||
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Sincerely, | Sincerely, | ||
/RA/ | /RA/ | ||
Eric R. Duncan, Chief Branch 4 Division of Reactor Projects Docket Nos. 05000315 and 05000316 License Nos. DPR-58 and DPR-74 | |||
Eric R. Duncan, Chief Branch 4 Division of Reactor Projects | |||
Docket Nos. 05000315 and 05000316 License Nos. DPR-58 and DPR-74 | |||
===Enclosure:=== | ===Enclosure:=== | ||
As stated | As stated | ||
==Inspection Report== | ==Inspection Report== | ||
Docket Numbers: 05000315 and 05000316 License Numbers: DPR-58 and DPR-74 Report Numbers: 05000315/2019003 and 05000316/2019003 Enterprise Identifier: I-2019-003-0068 Licensee: Indiana Michigan Power Company Facility: Donald C. Cook Nuclear Plant, Units 1 and 2 Location: Bridgman, MI Inspection Dates: July 01, 2019 to September 30, 2019 Inspectors: J. Ellegood, Senior Resident Inspector N. Feliz-Adorno, Senior Reactor Inspector T. Go, Health Physicist P. Laflamme, Senior Resident Inspector J. Mancuso, Resident Inspector R. Ng, Project Engineer J. Rutkowski, Project Engineer M. Ziolkowski, Senior Physical Security Inspector Approved By: Eric R. Duncan, Chief Branch 4 Division of Reactor Projects | Docket Numbers: | ||
05000315 and 05000316 | |||
License Numbers: | |||
DPR-58 and DPR-74 | |||
Report Numbers: | |||
05000315/2019003 and 05000316/2019003 | |||
Enterprise Identifier: I-2019-003-0068 | |||
Licensee: | |||
Indiana Michigan Power Company | |||
Facility: | |||
Donald C. Cook Nuclear Plant, Units 1 and 2 | |||
Location: | |||
Bridgman, MI | |||
Inspection Dates: | |||
July 01, 2019 to September 30, 2019 | |||
Inspectors: | |||
J. Ellegood, Senior Resident Inspector | |||
N. Feliz-Adorno, Senior Reactor Inspector | |||
T. Go, Health Physicist | |||
P. Laflamme, Senior Resident Inspector | |||
J. Mancuso, Resident Inspector | |||
R. Ng, Project Engineer | |||
J. Rutkowski, Project Engineer | |||
M. Ziolkowski, Senior Physical Security Inspector | |||
Approved By: | |||
Eric R. Duncan, Chief | |||
Branch 4 | |||
Division of Reactor Projects | |||
=SUMMARY= | =SUMMARY= | ||
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Donald C. Cook Nuclear Plant, Units 1 and 2 in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. | The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Donald C. Cook Nuclear Plant, Units 1 and 2 in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. | ||
List of Findings and Violations Main Steam Stop Valve Dump Valve Inoperable for Longer than its Technical Specification Allowed Outage Time Cornerstone | ===List of Findings and Violations=== | ||
Main Steam Stop Valve Dump Valve Inoperable for Longer than its Technical Specification Allowed Outage Time Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000315/2019003-01 Open/Closed | |||
[H.14] - | |||
Conservative Bias 71152 The inspectors identified a finding of very low safety significance (i.e., Green) and an associated Non-Cited Violation (NCV) of Technical Specification (TS) 3.7.2, Steam Generator Stop Valves (SGVSs), when licensee personnel failed to have four Unit 1 SGSVs and associated actuator trains operable while in Mode 1 and subsequently failed to restore the affected SGSV actuator train and SGSV to an operable status or place Unit 1 in Mode 2 within the time limits specified by the associated TS Limiting Condition for Operation (LCO). In addition, a NCV of TS 3.0.4, LCO Applicability, was identified because the licensee entered a Mode of applicability without the SGSV actuator train and associated SGSV being operable as required. Specifically, the licensee failed to identify that Unit 1 #2 SGVS Train B Dump Valve MRV-222 was inoperable during a post-maintenance test (PMT) conducted on May 6, 2019; and subsequently entered Mode 1 contrary to TS 3.0.4 and operated for 21 days, contrary to TS 3.7.2. | |||
Additional Tracking Items Type | ===Additional Tracking Items=== | ||
Type Issue Number Title Report Section Status URI 05000315,05000316/20 18003-02 Site Specific Shielding and Barriers for HI-TRAC Transfer Cask Require NRC Approval Prior to Use 60855.1 Closed | |||
=PLANT STATUS= | =PLANT STATUS= | ||
| Line 66: | Line 116: | ||
==REACTOR SAFETY== | ==REACTOR SAFETY== | ||
==71111.01 - Adverse Weather Protection== | |||
==71111.01 - Adverse Weather Protection External Flooding Sample (IP Section 03.04)== | ===External Flooding Sample (IP Section 03.04) (1 Sample)=== | ||
: (1) The inspectors evaluated the licensee's readiness to cope with external flooding for the following area: | : (1) The inspectors evaluated the licensee's readiness to cope with external flooding for the following area: | ||
* Screen House | * Screen House | ||
==71111.04Q - Equipment Alignment Partial Walkdown Sample (IP Section 03.01)== | ==71111.04Q - Equipment Alignment== | ||
===Partial Walkdown Sample (IP Section 03.01) (5 Samples)=== | |||
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains: | The inspectors evaluated system configurations during partial walkdowns of the following systems/trains: | ||
: (1) Unit 1 Emergency Diesel Generator (EDG) AB and Associated Support Systems on July 8, 2019 | : (1) Unit 1 Emergency Diesel Generator (EDG) AB and Associated Support Systems on July 8, 2019 | ||
| Line 82: | Line 130: | ||
: (5) Unit 2 CD EDG on August 21, 2019 | : (5) Unit 2 CD EDG on August 21, 2019 | ||
==71111.04S - Equipment Alignment Complete Walkdown Sample (IP Section 03.02)== | ==71111.04S - Equipment Alignment== | ||
===Complete Walkdown Sample (IP Section 03.02) (1 Sample)=== | |||
: (1) The inspectors evaluated system configurations during a complete walkdown of the Unit 1 Qualified Offsite Power Lines on September 23, 2019 | : (1) The inspectors evaluated system configurations during a complete walkdown of the Unit 1 Qualified Offsite Power Lines on September 23, 2019 | ||
==71111.05Q - Fire Protection Quarterly Inspection (IP Section 03.01)== | ==71111.05Q - Fire Protection== | ||
===Quarterly Inspection (IP Section 03.01) (4 Samples)=== | |||
The inspectors evaluated fire protection program implementation in the following selected areas: | The inspectors evaluated fire protection program implementation in the following selected areas: | ||
: (1) U2 CD EDG on July 7, 2019 | : (1) U2 CD EDG on July 7, 2019 | ||
| Line 95: | Line 142: | ||
: (4) U2 4 Kilovolt (kV) Switchgear Rooms AB and CD on July 11, 2019 | : (4) U2 4 Kilovolt (kV) Switchgear Rooms AB and CD on July 11, 2019 | ||
==71111.06 - Flood Protection Measures Inspection Activities - Internal Flooding (IP Section 02.02a.)== | ==71111.06 - Flood Protection Measures== | ||
===Inspection Activities - Internal Flooding (IP Section 02.02a.) (1 Sample)=== | |||
The inspectors evaluated internal flooding mitigation protection in the: | The inspectors evaluated internal flooding mitigation protection in the: | ||
: (1) Auxiliary Building, Elevations 573' and 587' | : (1) Auxiliary Building, Elevations 573' and 587' | ||
==71111.07A - Heat Sink Performance Annual Review (IP Section 02.01)== | ==71111.07A - Heat Sink Performance== | ||
===Annual Review (IP Section 02.01) (1 Sample)=== | |||
The inspectors evaluated readiness and performance of: | The inspectors evaluated readiness and performance of: | ||
: (1) Unit 2 Non-Essential Service Water (NESW) | : (1) Unit 2 Non-Essential Service Water (NESW) | ||
==71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) | ==71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance== | ||
Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample) | |||
: (1) The inspectors observed and evaluated licensed operator performance in the Control Room during a plant shutdown for a maintenance outage on July 21, 2019 Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample) | : (1) The inspectors observed and evaluated licensed operator performance in the Control Room during a plant shutdown for a maintenance outage on July 21, 2019 | ||
===Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)=== | |||
: (1) The inspectors observed and evaluated licensed operator requalification training in the Unit 2 Simulator on September 12, 2019 | : (1) The inspectors observed and evaluated licensed operator requalification training in the Unit 2 Simulator on September 12, 2019 | ||
==71111.12 - Maintenance Effectiveness Routine Maintenance Effectiveness Inspection (IP Section 02.01)== | ==71111.12 - Maintenance Effectiveness== | ||
===Routine Maintenance Effectiveness Inspection (IP Section 02.01) (3 Samples)=== | |||
The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions: | The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions: | ||
: (1) Unit 1 Auxiliary Feedwater (AFW) | : (1) Unit 1 Auxiliary Feedwater (AFW) | ||
| Line 120: | Line 166: | ||
: (3) Supplemental Emergency Diesel Generators (EDGs) | : (3) Supplemental Emergency Diesel Generators (EDGs) | ||
==71111.13 - Maintenance Risk Assessments and Emergent Work Control Risk Assessment and Management Sample (IP Section 03.01)== | ==71111.13 - Maintenance Risk Assessments and Emergent Work Control== | ||
===Risk Assessment and Management Sample (IP Section 03.01) (2 Samples)=== | |||
The inspectors evaluated the risk assessments for the following planned and emergent work activities: | The inspectors evaluated the risk assessments for the following planned and emergent work activities: | ||
: (1) Elevated Risk due to unplanned Unit 1 AB EDG inoperability on June 17, 2019 | : (1) Elevated Risk due to unplanned Unit 1 AB EDG inoperability on June 17, 2019 | ||
: (2) Elevated Risk associated with the loss of Unit 2 NESW from July 21 through July 24, 2019 | : (2) Elevated Risk associated with the loss of Unit 2 NESW from July 21 through July 24, 2019 | ||
==71111.15 - Operability Determinations and Functionality Assessments Operability Determination or Functionality Assessment (IP Section 02.02)== | ==71111.15 - Operability Determinations and Functionality Assessments== | ||
===Operability Determination or Functionality Assessment (IP Section 02.02) (5 Samples)=== | |||
The inspectors evaluated the following operability determinations and functionality assessments: | The inspectors evaluated the following operability determinations and functionality assessments: | ||
: (1) AR 2015-5237, Asymmetric Natural Circulation Cooldown with Low Decay Heat | : (1) AR 2015-5237, Asymmetric Natural Circulation Cooldown with Low Decay Heat | ||
| Line 137: | Line 181: | ||
: (5) Step Change in Differential Pressure (D/P) Across Auxiliary Fuel Handling Area Exhaust Filter | : (5) Step Change in Differential Pressure (D/P) Across Auxiliary Fuel Handling Area Exhaust Filter | ||
==71111.19 - Post-Maintenance Testing Post-Maintenance Test Sample (IP Section 03.01)== | ==71111.19 - Post-Maintenance Testing== | ||
===Post-Maintenance Test Sample (IP Section 03.01) (6 Samples)=== | |||
The inspectors evaluated the following post maintenance tests: | The inspectors evaluated the following post maintenance tests: | ||
: (1) Mechanism-Operated Contact Switch Adjustment for Unit 1 AB EDG to 4kV Bus Supply Breaker; Work Order (WO) 55535235 | : (1) Mechanism-Operated Contact Switch Adjustment for Unit 1 AB EDG to 4kV Bus Supply Breaker; Work Order (WO) 55535235 | ||
| Line 146: | Line 189: | ||
: (4) Unit 1 CD EDG, on August 29, 2019, following planned maintenance | : (4) Unit 1 CD EDG, on August 29, 2019, following planned maintenance | ||
: (5) Unit 1 TDAFW System on September 3, 2019, following planned maintenance | : (5) Unit 1 TDAFW System on September 3, 2019, following planned maintenance | ||
: (6) Unit 1 East Component Cooling Water (CCW) Check Valve Flow Test following RCP | : (6) Unit 1 East Component Cooling Water (CCW) Check Valve Flow Test following RCP | ||
#3 Lower Bearing CCW Throttle Valve Adjustment on September 13, 2019 | |||
==71111.20 - Refueling and Other Outage Activities Refueling/Other Outage Sample (IP Section 03.01)== | ==71111.20 - Refueling and Other Outage Activities== | ||
===Refueling/Other Outage Sample (IP Section 03.01) (1 Sample)=== | |||
: (1) The inspectors evaluated a Unit 2 maintenance outage from July 21 through July 25, 2019, which resulted from accumulated debris in the NESW strainers | : (1) The inspectors evaluated a Unit 2 maintenance outage from July 21 through July 25, 2019, which resulted from accumulated debris in the NESW strainers | ||
==71111.22 - Surveillance Testing The inspectors evaluated the following surveillance test: | ==71111.22 - Surveillance Testing== | ||
Surveillance Tests (other) (IP Section 03.01)== | The inspectors evaluated the following surveillance test: | ||
===Surveillance Tests (other) (IP Section 03.01)=== | |||
{{IP sample|IP=IP 71111.22|count=1}} | {{IP sample|IP=IP 71111.22|count=1}} | ||
: (1) Unit 2 New Fuel Receipt Inspections; WO 55518169 and WO 55518412 | : (1) Unit 2 New Fuel Receipt Inspections; WO 55518169 and WO 55518412 | ||
=== | ==71114.06 - Drill Evaluation== | ||
Select Emergency Preparedness Drills and/or Training for Observation (IP Section 03.01) (1 Sample) | |||
: (1) Emergency Preparedness Drill on July 16, 2019 | |||
===Drill/Training Evolution Observation (IP Section 03.02) (1 Sample)=== | |||
The inspectors evaluated: | The inspectors evaluated: | ||
: (1) Licensed Operator Requalification Training (LORT) with Drill Exercise Performance (DEP) on September 10, | : (1) Licensed Operator Requalification Training (LORT) with Drill Exercise Performance (DEP) on September 10, | ||
==RADIATION SAFETY== | ==RADIATION SAFETY== | ||
==71124.08 - Radioactive Solid Waste Processing and Radioactive Material Handling, Storage,== | |||
and Transportation | |||
== | ===Radioactive Material Storage (IP Section 02.01)=== | ||
{{IP sample|IP=IP 71124.08|count=1}} | {{IP sample|IP=IP 71124.08|count=1}} | ||
| Line 178: | Line 224: | ||
* South Boric-Acid Evaporator Room 587 | * South Boric-Acid Evaporator Room 587 | ||
* Radioactive Material Building and Contaminated Equipment Storage Area (CESA) Building where Dry Active Waste (DAW) Containers were Stored | * Radioactive Material Building and Contaminated Equipment Storage Area (CESA) Building where Dry Active Waste (DAW) Containers were Stored | ||
* Mausoleum Storage Area and CESA Contains Contaminated Equipment Stored in Sea-Lands The inspectors performed a container check (e.g., swelling, leakage and deformation)on the following containers: | * Mausoleum Storage Area and CESA Contains Contaminated Equipment Stored in Sea-Lands | ||
The inspectors performed a container check (e.g., swelling, leakage and deformation)on the following containers: | |||
* DAW Container No. 321; Air Compressors; dated February 19, 2013 | * DAW Container No. 321; Air Compressors; dated February 19, 2013 | ||
* DAW Container No. 314; Stinger Whip Welding Equipment; dated July 27, 2017 | * DAW Container No. 314; Stinger Whip Welding Equipment; dated July 27, 2017 | ||
| Line 186: | Line 234: | ||
* DAW Container No. 324; Power Packs and Electrical Transformers; dated March 14, 2016 | * DAW Container No. 324; Power Packs and Electrical Transformers; dated March 14, 2016 | ||
* DAW Container No. 226; Specimen Tools/Bolts for CRD Tools; dated April 28, 2019 | * DAW Container No. 226; Specimen Tools/Bolts for CRD Tools; dated April 28, 2019 | ||
* DAW Container No. 237; CRDM [Control Rod Drive Mechanism] Equipment Radioactive Waste System Walkdown (IP Section 02.02) (1 Sample) | * DAW Container No. 237; CRDM [Control Rod Drive Mechanism] Equipment | ||
===Radioactive Waste System Walkdown (IP Section 02.02) (1 Sample)=== | |||
The inspectors evaluated the following radioactive waste processing systems during plant walkdowns: | The inspectors evaluated the following radioactive waste processing systems during plant walkdowns: | ||
: (1) Liquid or Solid Radioactive Waste Processing Systems | : (1) Liquid or Solid Radioactive Waste Processing Systems | ||
| Line 192: | Line 242: | ||
* Energy Solution Liquid System; Radioactive Waste Water Demineralizer System | * Energy Solution Liquid System; Radioactive Waste Water Demineralizer System | ||
* Spent Resin Storage Tank Resin Transfer System | * Spent Resin Storage Tank Resin Transfer System | ||
* DAW Trash Loading Located in the Auxiliary Building Radioactive Waste Resin and/or Sludge Discharges Processes | * DAW Trash Loading Located in the Auxiliary Building | ||
Radioactive Waste Resin and/or Sludge Discharges Processes | |||
* Energy Solutions Liquid System; Radioactive Waste Water Demineralizer System | * Energy Solutions Liquid System; Radioactive Waste Water Demineralizer System | ||
* Spent Resin Storage Tank Resin Transfer System Waste Characterization and Classification (IP Section 02.03) (1 Sample) | * Spent Resin Storage Tank Resin Transfer System | ||
===Waste Characterization and Classification (IP Section 02.03) (1 Sample)=== | |||
The inspectors evaluated the radioactive waste characterization and classification for the following waste streams: | The inspectors evaluated the radioactive waste characterization and classification for the following waste streams: | ||
: (1) Shipping Cask Containing Spent Resin to Bear Creek, TN; Low Specific Activity (LSA-II) | : (1) Shipping Cask Containing Spent Resin to Bear Creek, TN; Low Specific Activity (LSA-II) | ||
Contaminated Equipment RAM [Radioactive Material] Shipment to Energy Solution Services as Surface Contaminated Objects (SCO-II) | Contaminated Equipment RAM [Radioactive Material] Shipment to Energy Solution Services as Surface Contaminated Objects (SCO-II) | ||
Sample Shipment of 8 Samples to be Analyzed to GEL Laboratory as a Limited Quantity Material | Sample Shipment of 8 Samples to be Analyzed to GEL Laboratory as a Limited Quantity Material | ||
===Shipment Preparation (IP Section 02.04) (1 Sample)=== | ===Shipment Preparation (IP Section 02.04) (1 Sample)=== | ||
The inspectors evaluated the following radioactive material shipment preparation processes: | The inspectors evaluated the following radioactive material shipment preparation processes: | ||
: (1) DCC18-053; UN3321, RAM LSA-II; Fissile Excepted; 7, RQ-1; Spent Resin Mixed Bed Ion Exchange Media to Bear Creek, TN; dated July 12, 2018 DCC18-074; UN3321, RAM LSA-II; Fissile Excepted; 7, RQ-1; Spent Resin Mixed Bed Ion Exchange Media to Bear Creek, TN; dated December 5, 2018 DCC19-053; UN2913, RAM SCO-II; Fissile Excepted; 7, RQ-1; Contaminated Equipment Contained in a Metal Box to Energy Solution Services, Memphis, TN; dated June 11, 2019 | : (1) DCC18-053; UN3321, RAM LSA-II; Fissile Excepted; 7, RQ-1; Spent Resin Mixed Bed Ion Exchange Media to Bear Creek, TN; dated July 12, 2018 DCC18-074; UN3321, RAM LSA-II; Fissile Excepted; 7, RQ-1; Spent Resin Mixed Bed Ion Exchange Media to Bear Creek, TN; dated December 5, 2018 DCC19-053; UN2913, RAM SCO-II; Fissile Excepted; 7, RQ-1; Contaminated Equipment Contained in a Metal Box to Energy Solution Services, Memphis, TN; dated June 11, 2019 | ||
===Shipping Records (IP Section 02.05) (1 Sample)=== | ===Shipping Records (IP Section 02.05) (1 Sample)=== | ||
| Line 209: | Line 263: | ||
==OTHER ACTIVITIES - BASELINE== | ==OTHER ACTIVITIES - BASELINE== | ||
===71151 - Performance Indicator Verification | |||
The inspectors verified licensee performance indicators submittals listed below: | |||
BI01: Reactor Coolant System (RCS) Specific Activity Sample (IP Section 02.10) === | |||
BI01: Reactor Coolant System (RCS) Specific Activity Sample (IP Section 02.10)=== | |||
{{IP sample|IP=IP 71151|count=2}} | {{IP sample|IP=IP 71151|count=2}} | ||
: (1) PMP-7110-PIP-001; Reactor Oversight Program Performance Indicators (PIs) and Monthly Operating Report Data for Reactor Coolant Specific Activity; Unit 1; from January 1, 2018 through December 31, 2018 | : (1) PMP-7110-PIP-001; Reactor Oversight Program Performance Indicators (PIs) and Monthly Operating Report Data for Reactor Coolant Specific Activity; Unit 1; from January 1, 2018 through December 31, 2018 | ||
: (2) PMP-7110-PIP-001; Reactor Oversight Program PIs and Monthly Operating Report Data for Reactor Coolant Specific Activity; Unit 2; from January 1, 2018 through December 31, 2018 | : (2) PMP-7110-PIP-001; Reactor Oversight Program PIs and Monthly Operating Report Data for Reactor Coolant Specific Activity; Unit 2; from January 1, 2018 through December 31, 2018 | ||
==71152 - Problem Identification and Resolution Semiannual Trend Review (IP Section 02.02)== | ==71152 - Problem Identification and Resolution== | ||
===Semiannual Trend Review (IP Section 02.02) (1 Sample)=== | |||
: (1) The inspectors reviewed licensee Nuclear Oversight reports, Nuclear Safety Review Board (NSRB) reports, and System Health summaries to identify potential adverse trends in documented issues that were not entered into the licensees corrective action program. The inspectors also assessed NRC findings to identify trends. | : (1) The inspectors reviewed licensee Nuclear Oversight reports, Nuclear Safety Review Board (NSRB) reports, and System Health summaries to identify potential adverse trends in documented issues that were not entered into the licensees corrective action program. The inspectors also assessed NRC findings to identify trends. | ||
Annual Follow-up of Selected Issues (IP Section 02.03) (2 Samples 1 Partial) | Annual Follow-up of Selected Issues (IP Section 02.03) (2 Samples 1 Partial) | ||
The inspectors reviewed the licensees implementation of the corrective action program related to the following issues: | |||
The inspectors reviewed the licensees implementation of the corrective action program related to the following issues: | |||
(1) | |||
(Partial) | |||
Missing Lateral Support Shim for Reactor Coolant Pump (RCP)-11 | Missing Lateral Support Shim for Reactor Coolant Pump (RCP)-11 | ||
: (2) Through-Wall Leak on Unit 1 RCP Seal Injection Lines | : (2) Through-Wall Leak on Unit 1 RCP Seal Injection Lines | ||
| Line 228: | Line 287: | ||
==OTHER ACTIVITIES== | ==OTHER ACTIVITIES== | ||
- TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL 60855.1 - Operation of an Independent Spent Fuel Storage Installation at Operating Plants Operation of an Independent Spent Fuel Storage Installation at Operating Plants (1 Partial) | - TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL | ||
60855.1 - Operation of an Independent Spent Fuel Storage Installation at Operating Plants | |||
Operation of an Independent Spent Fuel Storage Installation at Operating Plants (1 Partial) | |||
(1) | |||
(Partial) | |||
The inspectors closed Unresolved Item 05000315/2018003-002; 05000316/2018003-02, Site Specific Shielding and Barriers for HI-TRAC Transfer Cask Require NRC Approval Prior to Use. The details of this review are documented in the inspection results below. No findings or violations were identified. | The inspectors closed Unresolved Item 05000315/2018003-002; 05000316/2018003-02, Site Specific Shielding and Barriers for HI-TRAC Transfer Cask Require NRC Approval Prior to Use. The details of this review are documented in the inspection results below. No findings or violations were identified. | ||
==INSPECTION RESULTS== | ==INSPECTION RESULTS== | ||
Unresolved Item | Unresolved Item (Closed) | ||
Site Specific Shielding and Barriers for HI-TRAC Transfer Cask Require NRC Approval Prior to Use URI 05000315,05000316/2018003-02 60855.1 | |||
=====Description:===== | =====Description:===== | ||
| Line 262: | Line 328: | ||
Since the licensee was compliant with CoC No. 1014, Amendment No. 9R1, Appendix B and 10 CFR 72.48, the inspectors consider this Unresolved Item closed. | Since the licensee was compliant with CoC No. 1014, Amendment No. 9R1, Appendix B and 10 CFR 72.48, the inspectors consider this Unresolved Item closed. | ||
Corrective Action References: AR 2018-4056, AR 2018-6342, and AR 2018-6642 Main Steam Stop Valve Dump Valve Inoperable for Longer than its Technical Specification Allowed Outage Time Cornerstone | Corrective Action References: AR 2018-4056, AR 2018-6342, and AR 2018-6642 Main Steam Stop Valve Dump Valve Inoperable for Longer than its Technical Specification Allowed Outage Time Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems | ||
Green NCV 05000315/2019003-01 Open/Closed | |||
[H.14] - | |||
Conservative Bias 71152 The inspectors identified a finding of very low safety significance (i.e., Green) and an associated Non-Cited Violation (NCV) of Technical Specification (TS) 3.7.2, Steam Generator Stop Valves (SGVSs), when licensee personnel failed to have four Unit 1 SGSVs and associated actuator trains operable while in Mode 1 and subsequently failed to restore the affected SGSV actuator train and SGSV to an operable status or place Unit 1 in Mode 2 within the time limits specified by the associated TS Limiting Condition for Operation (LCO). | |||
In addition, a NCV of TS 3.0.4, LCO Applicability, was identified because the licensee entered a Mode of applicability without the SGSV actuator train and associated SGSV being operable as required. Specifically, the licensee failed to identify that Unit 1 #2 SGVS Train B Dump Valve MRV-222 was inoperable during a post-maintenance test (PMT) conducted on May 6, 2019; and subsequently entered Mode 1 contrary to TS 3.0.4 and operated for 21 days, contrary to TS 3.7.2. | In addition, a NCV of TS 3.0.4, LCO Applicability, was identified because the licensee entered a Mode of applicability without the SGSV actuator train and associated SGSV being operable as required. Specifically, the licensee failed to identify that Unit 1 #2 SGVS Train B Dump Valve MRV-222 was inoperable during a post-maintenance test (PMT) conducted on May 6, 2019; and subsequently entered Mode 1 contrary to TS 3.0.4 and operated for 21 days, contrary to TS 3.7.2. | ||
| Line 275: | Line 346: | ||
Corrective Actions: The licensee performed a past operability assessment under AR 2019-8511. The deficient condition was corrected previously under AR 2019-5615 on May 30, 2019. | Corrective Actions: The licensee performed a past operability assessment under AR 2019-8511. The deficient condition was corrected previously under AR 2019-5615 on May 30, 2019. | ||
Corrective Action References: AR 2019-5615 | Corrective Action References: AR 2019-5615 | ||
=====Performance Assessment:===== | =====Performance Assessment:===== | ||
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Significance: The inspectors assessed the significance of the finding using Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The inspectors answered Yes to Question A.2 in Exhibit 2 because the Unit 1 #2 SGSV Train B Dump Valve was inoperable for 21 days, which was greater than the TS 3.7.2 Allowed Outage Time of 7 days. | Significance: The inspectors assessed the significance of the finding using Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The inspectors answered Yes to Question A.2 in Exhibit 2 because the Unit 1 #2 SGSV Train B Dump Valve was inoperable for 21 days, which was greater than the TS 3.7.2 Allowed Outage Time of 7 days. | ||
Therefore, a Detailed Risk Evaluation (DRE) was performed using Inspection Manual Chapter (IMC) 0609, Appendix A. The inspectors performed a bounding analysis by failing the Unit 1 | Therefore, a Detailed Risk Evaluation (DRE) was performed using Inspection Manual Chapter (IMC) 0609, Appendix A. The inspectors performed a bounding analysis by failing the Unit 1 | ||
#2 SGSV Train B Dump Valve for 21 days and determined the delta core damage frequency (CDF) was 4.7E-9. As a result, the finding was determined to be of very low safety significance (i.e., Green). | #2 SGSV Train B Dump Valve for 21 days and determined the delta core damage frequency (CDF) was 4.7E-9. As a result, the finding was determined to be of very low safety significance (i.e., Green). | ||
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=DOCUMENTS REVIEWED= | =DOCUMENTS REVIEWED= | ||
Inspection Type | Inspection | ||
Procedure | |||
71111.04Q Corrective Action 2018-0075 | Type | ||
Designation | |||
2018-6841 | Description or Title | ||
2018-6917 | Revision or | ||
2018-9194 | Date | ||
Drawings | 71111.04Q Corrective Action | ||
OP-1-5113A-9 | Documents | ||
OP-1-5143-80 | 2018-0075 | ||
OP-1-5148C-30 | U1 CD EDG Tripped Due to Air System Issues | ||
01/02/2018 | |||
2018-0242 | |||
DG1CD Tripped on Overspeed During a Start | |||
01/08/2018 | |||
2018-6841 | |||
Unit 1 CD EDG Not Synchronizing to T11D Bus | |||
07/02/2018 | |||
2018-6917 | |||
Potential Commonality in Recent Repeat Events | |||
07/05/2018 | |||
2018-9194 | |||
Unit 2 PAC Trip | |||
09/27/2018 | |||
Drawings | |||
1-OP-5151D-72 | |||
Flow Diagram Emergency Diesel Generator CD Unit 1 | |||
OP-1-5113A-9 | |||
Flow Diagram Essential Service Water | |||
OP-1-5143-80 | |||
Flow Diagram Emergency Core Cooling (RHR) Unit No. 1 | |||
OP-1-5148C-30 | |||
Flow Diagram Diesel Generator Area & Electric Switchgear | |||
Room Heating & Ventilation System Unit 1 | Room Heating & Ventilation System Unit 1 | ||
OP-1-5151A-50 | OP-1-5151A-50 | ||
OP-1-5151C-58 | Flow Diagram Emergency Diesel Generator AB Unit 1 | ||
OP-1-98013-42 | OP-1-5151C-58 | ||
OP-1-98014-40 | Flow Diagram Emergency Diesel Generator CD Unit 1 | ||
OP-1-98016-41 | OP-1-98013-42 | ||
Diesel Generator 1AB and Auxiliaries Elementary Diagram | |||
OP-1-98014-40 | |||
Diesel Generator 1CD and Auxiliaries Elementary Diagram | |||
OP-1-98016-41 | |||
Diesel Generator 1AB Miscellaneous Auxiliaries Elementary | |||
Diagram | Diagram | ||
OP-1-98017-46 | OP-1-98017-46 | ||
Diesel Generator 1CD Miscellaneous Auxiliaries Elementary | |||
Diagram | Diagram | ||
OP-2-5143-75 | OP-2-5143-75 | ||
OP-5151B-61 | Flow Diagram Emergency Core Cooling (RHR) Unit No. 2 | ||
Procedures | OP-5151B-61 | ||
Flow Diagram Emergency Diesel Generator AB Unit #1 | |||
Procedures | |||
1-OHP-4012-032- | |||
008CD | 008CD | ||
1-OHP-4021-008- Placing Emergency Core Cooling System in Standby | Operating DG1CD Subsystems | ||
1-OHP-4021-008- | |||
1-OHP-4021-017- | 2 | ||
Placing Emergency Core Cooling System in Standby | |||
Readiness | |||
1-OHP-4021-017- | |||
001 | 001 | ||
1-OHP-4021-032- | Operation of the Residual Heat Removal System | ||
1-OHP-4021-032- | |||
008AB | 008AB | ||
1-OHP-4021-032- | Operation DG1AB Subsystems | ||
1-OHP-4021-032- | |||
008B | 008B | ||
1-OHP-4030-156- | Operating DG1AB Subsystems | ||
1-OHP-4030-156- | |||
017E | 017E | ||
Inspection Type | East Motor Driven Auxiliary Feedwater System Test | ||
2-OHP-4021-008- Placing Emergency Core Cooling System in Standby | Inspection | ||
Procedure | |||
Type | |||
Designation | |||
Description or Title | |||
Revision or | |||
Date | |||
2-OHP-4021-008- | |||
Placing Emergency Core Cooling System in Standby | |||
Readiness | Readiness | ||
2-OHP-4021-032- Operating DG2CD Subsystems - DG2CD Starting Air | 2-OHP-4021-032- | ||
008CD | |||
2-OHP-4021-07- | Operating DG2CD Subsystems - DG2CD Starting Air | ||
System Valves | |||
2-OHP-4021-07- | |||
001 | 001 | ||
2-OHP-4030-256- | Operation of the Residual Heat Removal System | ||
2-OHP-4030-256- | |||
017T | 017T | ||
Work Orders | Turbine Driven Auxiliary Feedwater System Test | ||
71111.05Q Drawings | Work Orders | ||
2-5974 | 55501397 | ||
Fire Plans | MTRI, 2-PPS-1, Calibrate/Replace as Necessary | ||
Fire Zone 18 | 71111.05Q Drawings | ||
Fire Zone 40A | 2-5972 | ||
Fire Zone 47A | Fire Hazards Analysis Plan Below Basement Units 1 and 2 | ||
71111.06 | 2-5974 | ||
Fire Hazard Analysis Mezzanine Floor El. 609 Units 1 & 2 | |||
PRA-Flood-002 | Fire Plans | ||
PRA-Flood-004 | Fire Pre-Plans Volume 1 | ||
PRA-Flood-008 | Fire Zone 18 | ||
PRA-Flood-008 | CD Diesel Generator Room, Unit 2 Elevation 587 | ||
Fire Zone 40A | |||
kV AB Switchgear Room, Unit 1 Elevation 609-0 | |||
Fire Zone 47A | |||
4kV AB Switchgear Room, Unit 2 Elevation 609-0 | |||
71111.06 | |||
Calculations | |||
MD-12-Flood- | |||
008-N | |||
Flooding Due to Groundwater Level Increase, Cook Nuclear | |||
Plant Flood Hazard Re-Evaluation | |||
PRA-Flood-002 | |||
Internal Flooding Impact on Plant Power Distribution | |||
PRA-Flood-004 | |||
Internal Flooding - Qualitative Screening Analysis | |||
PRA-Flood-008 | |||
Flood Sources and Associated Flood Mechanisms | |||
PRA-Flood-008 | |||
Appendix F | Appendix F | ||
SD-061206-001 | Rupture Flow Rates of Flood Sources | ||
SD-061206-001 | |||
Flooding Evaluation Report for D.C. Cook Nuclear Power | |||
Plant | Plant | ||
Corrective Action | Corrective Action | ||
Documents | Documents | ||
Drawings | GT-2015-5625-23 Inspection Frequency for Interim Flood Measures | ||
OP-12-5123 | 08/12/2015 | ||
Procedures | Drawings | ||
2-EHP-4075- | OP-1-5123A | ||
Station Drainage - Auxiliary Building, Unit 1 | |||
OP-12-5123 | |||
Station Drainage Auxiliary Building | |||
Procedures | |||
1-OHP-4022 | |||
ESW System/Rupture | |||
2-EHP-4075- | |||
TCA-001 | TCA-001 | ||
2-OHP-4027- | Operator Time Critical Actions | ||
2-OHP-4027- | |||
FSG-1501 | FSG-1501 | ||
Inspection Type | Flooding Response Deployment | ||
71111.07A | Inspection | ||
OP-2-5114-93 | Procedure | ||
Procedures | Type | ||
2-OHP-4021-028- Operation of the Containment Chilled Water System, | Designation | ||
Description or Title | |||
71111.11Q Miscellaneous | Revision or | ||
Date | |||
71111.07A | |||
Drawings | |||
OP-1-5114-152 | |||
Flow Diagram Non-Essential Service Water Unit No. 1 | |||
OP-2-5114-93 | |||
Flow Diagram Non-Essential Service Water Unit No. 2 | |||
Procedures | |||
1-OHP-4022 | |||
NESW System Loss/Rupture | |||
2-OHP-4021-028- | |||
018 | |||
Operation of the Containment Chilled Water System, | |||
Figure 1, System Drawings | |||
71111.11Q Miscellaneous | |||
RQ-C-4431 | |||
Secondary Side Break & Pressurized Thermal Shock | |||
Analysis | Analysis | ||
SOER 87-3 | SOER 87-3 | ||
Pipe Failures in High Energy Systems Due to Erosion | |||
Corrosion | Corrosion | ||
71111.12 | 04/02/1987 | ||
71111.12 | |||
Corrective Action | |||
Documents | Documents | ||
Miscellaneous | 2019-5615-1 | ||
1-MRV-222 Failed Surveillance | |||
05/29/2019 | |||
Miscellaneous | |||
Two-year Unavailability Report for the Supplemental Diesel | |||
Generator (SDG) System; SSC 12-SDG | Generator (SDG) System; SSC 12-SDG | ||
71111.15 | 09/25/2019 | ||
71111.15 | |||
Calculations | |||
DC-D-01-CS-4 | |||
Piping and Pipe Support Analysis of CS and RC System for | |||
EBASCO Walkdown Package Nos. CS-11 and RC-09 | EBASCO Walkdown Package Nos. CS-11 and RC-09 | ||
Corrective Action 2018-6093 | Corrective Action | ||
Documents | |||
2018-7570-01 | 2018-6093 | ||
Increasing Unit 1 CCW Out-Leakage | |||
06/06/2018 | |||
2018-6615 | |||
Unidentified HELB Break Locations | |||
06/26/2018 | |||
2018-7570-01 | |||
Operability Determination Evaluation (Unit 1 East CCW Heat | |||
Exchanger Leak) | Exchanger Leak) | ||
2019-5237 | 07/27/2018 | ||
2019-5237 | |||
Asymmetrical Natural Circulation Cooldown Issue with Low | |||
Decay Heat | Decay Heat | ||
2019-5666 | 05/14/2019 | ||
2019-7053 | 2019-5666 | ||
AR 2019-6882 | Revise Procedure to Support TRM Update | ||
AR 2019-7919 | 05/30/2019 | ||
Drawings | 2019-7053 | ||
OP-1-5129 | Pressurizer Insurge/Outsurge | ||
OP-12-5148-63 | AR 2019-6882 | ||
Engineering | U2 Ice Bed Temps Above eSOMS Notification Limits | ||
07/15/2019 | |||
AR 2019-7919 | |||
2-HV-AFX Charcoal D/P Outside of ESOMS Limits | |||
08/19/2019 | |||
Drawings | |||
1-CS-780-L1-2 | |||
Containment | |||
OP-1-5129 | |||
CVCS-Reactor Letdown & Charging | |||
OP-12-5148-63 | |||
Flow Diagram Auxiliary Building Ventilation Units 1 & 2 | |||
Engineering | |||
Changes | |||
0000055754 | |||
Install Mechanical Jumper to Connect the Essential Service | |||
Water System to the Component Cooling Water System in | |||
Either Unit to Provide a Source of Makeup Water to the | Either Unit to Provide a Source of Makeup Water to the | ||
CCW System | CCW System | ||
Miscellaneous | Miscellaneous | ||
Temporary | FHA Exhaust Fan Charcoal Differential Pressure | ||
Inspection Type | 08/23/2019 | ||
Temporary | |||
Modification 12- Service Water System to the Component Cooling Water | Design, Install Mechanical Jumper to Connect the Essential | ||
Inspection | |||
Procedure | |||
Type | |||
Designation | |||
Description or Title | |||
Revision or | |||
Date | |||
Modification 12- | |||
TM-15-49 | |||
Service Water System to the Component Cooling Water | |||
System in Either Unit to Provide a Source of Makeup Water | |||
to the CCW System | to the CCW System | ||
UFSAR Section | UFSAR Section | ||
14.2.5 | 14.2.5 | ||
WCAP-14717 | Rupture of a Steam Pipe | ||
WCAP-14717 | |||
Evaluation of the Effects of Insurge/Outsurge Out-of-Limit | |||
Transients on the Integrity of the Pressurizer Program | Transients on the Integrity of the Pressurizer Program | ||
MUHP-5063 Summary Report | MUHP-5063 Summary Report | ||
Procedures | Procedures | ||
2-OHP-4021- | |||
016-003 | 016-003 | ||
2-OHP-5030- | Component Cooling Water System Operation | ||
2-OHP-5030- | |||
Work Orders | 016-001 | ||
Supply ESW to CCW for Makeup Using Temporary | |||
Modification | |||
Work Orders | |||
55504921-01 | |||
2-HV-AFX, Auxiliary Building Ventilation Fuel Handling | |||
Area Exhaust Filter Unit, Replace Charcoal Bed | Area Exhaust Filter Unit, Replace Charcoal Bed | ||
55504921-02 | 08/23/2017 | ||
55504921-02 | |||
2-HV-AFX, Auxiliary Building Ventilation Fuel Handling | |||
Area Exhaust Filter Unit, Perform Test After Charcoal | Area Exhaust Filter Unit, Perform Test After Charcoal | ||
Replacement | Replacement | ||
71111.18 | 08/28/2017 | ||
71111.19 | 71111.18 | ||
Procedures | |||
AR-2019-8528 | OHI-4016 | ||
Conduct of Operations: Guidelines | |||
71111.19 | |||
Corrective Action | |||
Documents | |||
2019-8353 | |||
Failed PMT 55533608-05, U1 CD Diesel has a Slight Leak | |||
on the 1-R Jacket Water Outlet | |||
08/30/2019 | |||
AR-2019-8528 | |||
Unit 1 East CCW Pump Surveillance was Aborted Due to #3 | |||
RCP CCW Flows | RCP CCW Flows | ||
Engineering | 09/06/2019 | ||
Engineering | |||
Miscellaneous | Evaluations | ||
DIT-B-03787-01 | |||
Restoration of Component Cooling Water Flow to Unit 1 | |||
Reactor Coolant Pump #3 Motor Bearing Cooler | |||
09/10/2019 | |||
Miscellaneous | |||
Clearance Order | |||
241552 | 241552 | ||
Procedures | 2-IMO-312 Actuator | ||
Procedures | |||
1-OHP-4030-116- | |||
20E | 20E | ||
1-OHP-4030-132- | East Component Cooling Water Loop Surveillance Test | ||
09/13/2019 | |||
2-OHP-4030-208- | 1-OHP-4030-132- | ||
27CD | |||
CD Diesel Generator Operability Test (Train A), DG1CD | |||
Fast Speed Start | |||
2-OHP-4030-208- | |||
053A | 053A | ||
Shipping Records | ECCS Valve Operability Test - Train A | ||
Work Orders | Shipping Records 55518412-11 | ||
Inspection Type | MTRS, (R2P) U2 Load New Fuel into SFP | ||
Work Orders | |||
55518169-01 | 55359920-10 | ||
55535360-14 | OPS: 2-IMO-312, Stroke for PMT Operability | ||
Inspection | |||
Procedure | |||
Type | |||
Designation | |||
Description or Title | |||
Revision or | |||
Date | |||
55518169-01 | |||
MTRS, (R2P) U2 Unload New 17x17 Fuel | |||
55535360-14 | |||
MTM, 2-OME-35N Open NESW PP Strainer and Check for | |||
Debris | Debris | ||
55535386-05 | 97/21/2019 | ||
55535386-05 | |||
2-OME-35S MTM: 2-OME-35S; Open NESW Strainer and | |||
Check for Debris | Check for Debris | ||
WO Task: | 07/22/2019 | ||
WO Task: | |||
55523374 01 | 55523374 01 | ||
71111.20 | 1-FMO-231/Perform A-Found Diagnostic | ||
Procedures | 71111.20 | ||
Miscellaneous | |||
Forced Outage Critical Path | |||
07/22/2019 | |||
Procedures | |||
PMP-2291-OLR- | |||
001 | |||
Technical Specification 3.0.4.b Risk Assessment Review | |||
and Approval Form for Transitioning Modes with an | |||
Intermediate Range Nuclear Instrument Inoperable | Intermediate Range Nuclear Instrument Inoperable | ||
71114.06 | 71114.06 | ||
2019 DC Cook | Miscellaneous | ||
2019 DC Cook DR1 Drill Manual | |||
07/30/2019 | |||
2019 DC Cook | |||
EMPE Manual | EMPE Manual | ||
DR2 Drill | DC Cook EMPE Drill | ||
07/16/2019 | |||
EP-S-19DR2 | DR2 Drill | ||
Procedures | Scenario Manual | ||
Dress Rehearsal 2 (Team 3) | |||
August 13, | |||
2019 | |||
EP-S-19DR2 | |||
2019 Dress Rehearsal #2 | |||
Procedures | |||
RMT-2080-TSC- | |||
001 | 001 | ||
RMT-2080-TSC- | Activation and Operation of the TSC | ||
RMT-2080-TSC- | |||
CHK-001 | CHK-001 | ||
RMT-2080-TSC- | Site Emergency Director List | ||
RMT-2080-TSC- | |||
CHK-009 | CHK-009 | ||
71124.08 | PET-Operations Checklist | ||
71124.08 | |||
Calculations | |||
PMP-2030-REC- | |||
001 | 001 | ||
PMP-2030-REC- | 2016 10CFR61 Scaling Factor Report | ||
11/08/2017 | |||
PMP-2030-REC- | |||
001 | 001 | ||
Engineering | 2017 10CFR61 Scaling Factor Report | ||
10/29/2018 | |||
Self-Assessments GT-2018-1675 | Engineering | ||
Evaluations | |||
Technical 3002 8- | |||
20A Cask | |||
Cask Handling Procedure for USDOT Spec 7A, Type-A | |||
Transportation Cask | |||
05/14/2018 | |||
Self-Assessments GT-2018-1675 | |||
Self Assessment of the Radwaste Program at DC Cook that | |||
Covers Radwaste Processing, Handling and Transportation | Covers Radwaste Processing, Handling and Transportation | ||
Shipping Records DCC18-043 | 08/30/2018 | ||
Shipping Records DCC18-043 | |||
Compactible Trash to Energy Solution Bear Creek Facility | |||
for Processing | for Processing | ||
DCC18-044 | 05/10/2018 | ||
Inspection Type | DCC18-044 | ||
A Box of Contaminated Equipment to Framatome, Inc. | |||
DCC18-059 | 05/16/2018 | ||
Inspection | |||
Procedure | |||
Type | |||
Designation | |||
Description or Title | |||
Revision or | |||
Date | |||
DCC18-059 | |||
Mixed Bed Ion Exchange Spent Resin for Processing to | |||
Energy Solution Bear Creek, Oak Ridge,TN | Energy Solution Bear Creek, Oak Ridge,TN | ||
DCC18-074 | 07/24/2018 | ||
DCC18-074 | |||
Mixed Bed Resin PRC-1M; Class -B Shipment; UN3321; | |||
LSA-II; RQ; Contained in a Shipping Cask Model 8-120B; to | LSA-II; RQ; Contained in a Shipping Cask Model 8-120B; to | ||
Energy Solution for processing | Energy Solution for processing | ||
DCC19-033 | 11/30/2018 | ||
DCC19-033 | |||
UN2910 Excepted Package Limited Quantity of Steel Drum | |||
for Part 61 Anlysis | for Part 61 Anlysis | ||
DCC19-038 | 04/15/2019 | ||
DCC19-038 | |||
Shipment of 2 Sea-Vans Containing Contaminated | |||
Equipment to Westinghouse | Equipment to Westinghouse | ||
DCC19-041 | 04/25/2019 | ||
DCC19-053 | DCC19-041 | ||
Compacted Contaminated Trash to Unitech Services, TN | |||
05/01/2019 | |||
DCC19-053 | |||
Sea-van on a Flatbed Trailer Containing a Shipment | |||
Consigned as UN2913, SCOII Fissile Excepted | Consigned as UN2913, SCOII Fissile Excepted | ||
71151 | 06/11/2019 | ||
71151 | |||
Calculations | |||
PMP-7110-PIP- | |||
001 | |||
Reactor Oversight Program Performance Indicators and | |||
Monthly Operating Report Data for Reactor Coolant Specific | |||
Activity; Unit 1 and 2 | Activity; Unit 1 and 2 | ||
71152 | 01/01/2018 - | ||
2/31/2018 | |||
2019-4341 | 71152 | ||
2019-4734 | Corrective Action | ||
2019-4895 | Documents | ||
2019-5615 | 2019-2963 | ||
2019-8511 | Investigate Reactor Coolant Pump Seal Injection Line Under | ||
Miscellaneous | Suspicious Boric Acid Deposit | ||
03/22/2019 | |||
2019-4341 | |||
Failure to Verify Procedure Directed Terminal Points | |||
04/24/2019 | |||
2019-4734 | |||
Labeling in Unit 1 Lube Oil Tank Room Junction Box | |||
05/03/2019 | |||
2019-4895 | |||
1-MRV-222 Failed Post Maintenance Test Timing | |||
05/06/2019 | |||
2019-5615 | |||
1-MRV-222 Failed Surveillance | |||
05/29/2019 | |||
2019-8511 | |||
Past Operability Determination Possible Missed | |||
09/05/2019 | |||
Miscellaneous | |||
Outage Control Center Shift Package | |||
09/30/2019 | |||
Indiana Michigan Power 2019 Second Quarter Trend Report | Indiana Michigan Power 2019 Second Quarter Trend Report | ||
AEP-19-005 | AEP-19-005 | ||
NOS-19-002 | Donald C. Cook Nuclear Plant Safety Review Board Meeting | ||
03/04/2019 | |||
NOS-19-002 | |||
Nuclear Oversight Quarterly Report for October - December | |||
2018 | 2018 | ||
NOS-19-006 | 01/21/2019 | ||
NOS-19-006 | |||
Nuclear Oversight Quarterly Report for January - March | |||
2019 | 2019 | ||
UCR 2215 | 04/23/2019 | ||
UCR 2215 | |||
UFSAR Change Request, Data Sheet 1 of PMP-2350-SAR- | |||
001, UFSAR Update Process | 001, UFSAR Update Process | ||
Procedures | Procedures | ||
1-IHP-6040-171- | |||
001 | 001 | ||
Verification of Turbine Support Systems Interlocks | |||
20 | 20 | ||
}} | }} | ||
Latest revision as of 01:41, 2 January 2025
| ML19312A445 | |
| Person / Time | |
|---|---|
| Site: | Cook |
| Issue date: | 11/07/2019 |
| From: | Eric Duncan Reactor Projects Region 3 Branch 4 |
| To: | Gebbie J Indiana Michigan Power Co |
| References | |
| IR 2019003 | |
| Download: ML19312A445 (23) | |
Text
November 7, 2019
SUBJECT:
DONALD C. COOK NUCLEAR PLANT, UNITS 1 AND 2 - INTEGRATED INSPECTION REPORT 05000315/2019003 AND 05000316/2019003
Dear Mr. Gebbie:
On September 30, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Donald C. Cook Nuclear Plant, Units 1 and 2. On October 15, 2019, the NRC inspectors discussed the results of this inspection with you and other members of your staff.
The results of this inspection are documented in the enclosed report.
One finding of very low safety significance (Green) is documented in this report. This finding involved a violation of NRC requirements. We are treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2 of the Enforcement Policy.
If you contest the violation or significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:
Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; the Director, Office of Enforcement; and the NRC Resident Inspector at D.C. Cook.
If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; and the NRC Resident Inspector at D.C. Cook. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely,
/RA/
Eric R. Duncan, Chief Branch 4 Division of Reactor Projects
Docket Nos. 05000315 and 05000316 License Nos. DPR-58 and DPR-74
Enclosure:
As stated
Inspection Report
Docket Numbers:
05000315 and 05000316
License Numbers:
Report Numbers:
05000315/2019003 and 05000316/2019003
Enterprise Identifier: I-2019-003-0068
Licensee:
Indiana Michigan Power Company
Facility:
Donald C. Cook Nuclear Plant, Units 1 and 2
Location:
Bridgman, MI
Inspection Dates:
July 01, 2019 to September 30, 2019
Inspectors:
J. Ellegood, Senior Resident Inspector
N. Feliz-Adorno, Senior Reactor Inspector
T. Go, Health Physicist
P. Laflamme, Senior Resident Inspector
J. Mancuso, Resident Inspector
R. Ng, Project Engineer
J. Rutkowski, Project Engineer
M. Ziolkowski, Senior Physical Security Inspector
Approved By:
Eric R. Duncan, Chief
Branch 4
Division of Reactor Projects
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Donald C. Cook Nuclear Plant, Units 1 and 2 in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.
List of Findings and Violations
Main Steam Stop Valve Dump Valve Inoperable for Longer than its Technical Specification Allowed Outage Time Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000315/2019003-01 Open/Closed
[H.14] -
Conservative Bias 71152 The inspectors identified a finding of very low safety significance (i.e., Green) and an associated Non-Cited Violation (NCV) of Technical Specification (TS) 3.7.2, Steam Generator Stop Valves (SGVSs), when licensee personnel failed to have four Unit 1 SGSVs and associated actuator trains operable while in Mode 1 and subsequently failed to restore the affected SGSV actuator train and SGSV to an operable status or place Unit 1 in Mode 2 within the time limits specified by the associated TS Limiting Condition for Operation (LCO). In addition, a NCV of TS 3.0.4, LCO Applicability, was identified because the licensee entered a Mode of applicability without the SGSV actuator train and associated SGSV being operable as required. Specifically, the licensee failed to identify that Unit 1 #2 SGVS Train B Dump Valve MRV-222 was inoperable during a post-maintenance test (PMT) conducted on May 6, 2019; and subsequently entered Mode 1 contrary to TS 3.0.4 and operated for 21 days, contrary to TS 3.7.2.
Additional Tracking Items
Type Issue Number Title Report Section Status URI 05000315,05000316/20 18003-02 Site Specific Shielding and Barriers for HI-TRAC Transfer Cask Require NRC Approval Prior to Use 60855.1 Closed
PLANT STATUS
Unit 1 began the inspection period at rated thermal power. On September 29, 2019, the licensee reduced power to about 55 percent to repair a leak on a feedwater pump casing.
Unit 1 remained at or near 55 percent power for the remainder of the inspection period.
Unit 2 operated at or near rated thermal power until July 21, 2019, when the licensee shut down the unit in response to a degradation of Non-Essential Service Water (NESW) flow.
On July 25, 2019, the licensee restarted Unit 2. Unit 2 reached rated thermal power on July 26, 2019, and remained at or near rated thermal power until September 9, 2019, when Unit 2 began coast down operations prior to a scheduled refueling outage. On September 29, 2019, the licensee reduced power to about 50 percent to perform Main Steam Safety Valve testing. Following this testing, Unit 2 remained at or near 50 percent power for the remainder of the inspection period.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
REACTOR SAFETY
71111.01 - Adverse Weather Protection
External Flooding Sample (IP Section 03.04) (1 Sample)
- (1) The inspectors evaluated the licensee's readiness to cope with external flooding for the following area:
- Screen House
71111.04Q - Equipment Alignment
Partial Walkdown Sample (IP Section 03.01) (5 Samples)
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
- (1) Unit 1 Emergency Diesel Generator (EDG) AB and Associated Support Systems on July 8, 2019
- (2) Unit 2 Residual Heat Removal (RHR) on July 23, 2019
- (3) Unit 2 Turbine Driven Auxiliary Feedwater (TDAFW) Pump on August 8, 2019
- (4) Unit 1 West Motor Driven Auxiliary Feedwater (MDAFW) Pump on August 14, 2019
- (5) Unit 2 CD EDG on August 21, 2019
71111.04S - Equipment Alignment
Complete Walkdown Sample (IP Section 03.02) (1 Sample)
- (1) The inspectors evaluated system configurations during a complete walkdown of the Unit 1 Qualified Offsite Power Lines on September 23, 2019
71111.05Q - Fire Protection
Quarterly Inspection (IP Section 03.01) (4 Samples)
The inspectors evaluated fire protection program implementation in the following selected areas:
- (1) U2 CD EDG on July 7, 2019
- (3) Auxiliary Building 573' Elevation on July 11, 2019
- (4) U2 4 Kilovolt (kV) Switchgear Rooms AB and CD on July 11, 2019
71111.06 - Flood Protection Measures
Inspection Activities - Internal Flooding (IP Section 02.02a.) (1 Sample)
The inspectors evaluated internal flooding mitigation protection in the:
- (1) Auxiliary Building, Elevations 573' and 587'
71111.07A - Heat Sink Performance
Annual Review (IP Section 02.01) (1 Sample)
The inspectors evaluated readiness and performance of:
- (1) Unit 2 Non-Essential Service Water (NESW)
71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance
Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)
- (1) The inspectors observed and evaluated licensed operator performance in the Control Room during a plant shutdown for a maintenance outage on July 21, 2019
Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)
- (1) The inspectors observed and evaluated licensed operator requalification training in the Unit 2 Simulator on September 12, 2019
71111.12 - Maintenance Effectiveness
Routine Maintenance Effectiveness Inspection (IP Section 02.01) (3 Samples)
The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:
- (1) Unit 1 Auxiliary Feedwater (AFW)
- (2) Unit 1 Main Feedwater
- (3) Supplemental Emergency Diesel Generators (EDGs)
71111.13 - Maintenance Risk Assessments and Emergent Work Control
Risk Assessment and Management Sample (IP Section 03.01) (2 Samples)
The inspectors evaluated the risk assessments for the following planned and emergent work activities:
- (2) Elevated Risk associated with the loss of Unit 2 NESW from July 21 through July 24, 2019
71111.15 - Operability Determinations and Functionality Assessments
Operability Determination or Functionality Assessment (IP Section 02.02) (5 Samples)
The inspectors evaluated the following operability determinations and functionality assessments:
- (1) AR 2015-5237, Asymmetric Natural Circulation Cooldown with Low Decay Heat
- (2) AR 2019-6882, Ice Condenser After Exceeding Notification Limit
- (3) AR 2019-7053, PZR [Pressurizer] Insurge/Outsurge
- (4) AR 2019-7919, Low Differential Pressure Across Fuel Handling Area Ventilation System Charcoal Bed
- (5) Step Change in Differential Pressure (D/P) Across Auxiliary Fuel Handling Area Exhaust Filter
71111.19 - Post-Maintenance Testing
Post-Maintenance Test Sample (IP Section 03.01) (6 Samples)
The inspectors evaluated the following post maintenance tests:
- (1) Mechanism-Operated Contact Switch Adjustment for Unit 1 AB EDG to 4kV Bus Supply Breaker; Work Order (WO) 55535235
- (2) Unit 2 NESW Strainers following Cleaning, July 21 through 23, 2019
- (3) Unit 2 East RHR Pump following Valve Work; WO 55359920
- (4) Unit 1 CD EDG, on August 29, 2019, following planned maintenance
- (5) Unit 1 TDAFW System on September 3, 2019, following planned maintenance
- (6) Unit 1 East Component Cooling Water (CCW) Check Valve Flow Test following RCP
- 3 Lower Bearing CCW Throttle Valve Adjustment on September 13, 2019
71111.20 - Refueling and Other Outage Activities
Refueling/Other Outage Sample (IP Section 03.01) (1 Sample)
- (1) The inspectors evaluated a Unit 2 maintenance outage from July 21 through July 25, 2019, which resulted from accumulated debris in the NESW strainers
71111.22 - Surveillance Testing
The inspectors evaluated the following surveillance test:
Surveillance Tests (other) (IP Section 03.01)
- (1) Unit 2 New Fuel Receipt Inspections; WO 55518169 and WO 55518412
71114.06 - Drill Evaluation
Select Emergency Preparedness Drills and/or Training for Observation (IP Section 03.01) (1 Sample)
- (1) Emergency Preparedness Drill on July 16, 2019
Drill/Training Evolution Observation (IP Section 03.02) (1 Sample)
The inspectors evaluated:
- (1) Licensed Operator Requalification Training (LORT) with Drill Exercise Performance (DEP) on September 10,
RADIATION SAFETY
71124.08 - Radioactive Solid Waste Processing and Radioactive Material Handling, Storage,
and Transportation
Radioactive Material Storage (IP Section 02.01)
The inspectors evaluated radioactive material storage.
- (1) The inspectors toured the following areas:
- Radioactive Waste Drumming Room located in the Auxiliary Building 587'
- Radioactive Waste Condensate Tanks South/North 587'
- South Boric-Acid Evaporator Room 587
- Radioactive Material Building and Contaminated Equipment Storage Area (CESA) Building where Dry Active Waste (DAW) Containers were Stored
- Mausoleum Storage Area and CESA Contains Contaminated Equipment Stored in Sea-Lands
The inspectors performed a container check (e.g., swelling, leakage and deformation)on the following containers:
- DAW Container No. 321; Air Compressors; dated February 19, 2013
- DAW Container No. 314; Stinger Whip Welding Equipment; dated July 27, 2017
- DAW Container No. 230; Spent Fuel Pool Tools and Spares; dated February 1, 2012
- DAW Container No. 323; Camera Cables; dated February 1, 2013
- DAW Container No. 102; Thimble Plugs Tools for Seal-Table; dated May 6, 2019
- DAW Container No. 324; Power Packs and Electrical Transformers; dated March 14, 2016
Radioactive Waste System Walkdown (IP Section 02.02) (1 Sample)
The inspectors evaluated the following radioactive waste processing systems during plant walkdowns:
- (1) Liquid or Solid Radioactive Waste Processing Systems
- Radioactove Waste Drumming Room located in the Auxiliary Building 587 Resin Transfer/Sluicing System into a Liner/Cask
- Energy Solution Liquid System; Radioactive Waste Water Demineralizer System
- Spent Resin Storage Tank Resin Transfer System
- DAW Trash Loading Located in the Auxiliary Building
Radioactive Waste Resin and/or Sludge Discharges Processes
- Energy Solutions Liquid System; Radioactive Waste Water Demineralizer System
- Spent Resin Storage Tank Resin Transfer System
Waste Characterization and Classification (IP Section 02.03) (1 Sample)
The inspectors evaluated the radioactive waste characterization and classification for the following waste streams:
- (1) Shipping Cask Containing Spent Resin to Bear Creek, TN; Low Specific Activity (LSA-II)
Contaminated Equipment RAM [Radioactive Material] Shipment to Energy Solution Services as Surface Contaminated Objects (SCO-II)
Sample Shipment of 8 Samples to be Analyzed to GEL Laboratory as a Limited Quantity Material
Shipment Preparation (IP Section 02.04) (1 Sample)
The inspectors evaluated the following radioactive material shipment preparation processes:
- (1) DCC18-053; UN3321, RAM LSA-II; Fissile Excepted; 7, RQ-1; Spent Resin Mixed Bed Ion Exchange Media to Bear Creek, TN; dated July 12, 2018 DCC18-074; UN3321, RAM LSA-II; Fissile Excepted; 7, RQ-1; Spent Resin Mixed Bed Ion Exchange Media to Bear Creek, TN; dated December 5, 2018 DCC19-053; UN2913, RAM SCO-II; Fissile Excepted; 7, RQ-1; Contaminated Equipment Contained in a Metal Box to Energy Solution Services, Memphis, TN; dated June 11, 2019
Shipping Records (IP Section 02.05) (1 Sample)
The inspectors evaluated the following non-excepted package shipment records:
- (1) DCC18-059; UN3321, RAM LSA-II; Fissile Excepted; 7, RQ-1; Spent Resin Mixed Bed Ion Exchange Media to Bear Creek, TN in a Type-A Cask; dated June 11, 2019 DCC18-023; UN2910, RAM; Excepted Package; 7, Limited Quantity Material to GEL Labs; Containing Samples for 10CFR61 Analysis; dated March 18, DCC18-019; UN2910, RAM; Excepted Package; 7, Limited Quantity Material of Valves to Spartanburg, SC for Recertification; dated March 11,
OTHER ACTIVITIES - BASELINE
===71151 - Performance Indicator Verification
The inspectors verified licensee performance indicators submittals listed below:
BI01: Reactor Coolant System (RCS) Specific Activity Sample (IP Section 02.10)===
- (1) PMP-7110-PIP-001; Reactor Oversight Program Performance Indicators (PIs) and Monthly Operating Report Data for Reactor Coolant Specific Activity; Unit 1; from January 1, 2018 through December 31, 2018
- (2) PMP-7110-PIP-001; Reactor Oversight Program PIs and Monthly Operating Report Data for Reactor Coolant Specific Activity; Unit 2; from January 1, 2018 through December 31, 2018
71152 - Problem Identification and Resolution
Semiannual Trend Review (IP Section 02.02) (1 Sample)
- (1) The inspectors reviewed licensee Nuclear Oversight reports, Nuclear Safety Review Board (NSRB) reports, and System Health summaries to identify potential adverse trends in documented issues that were not entered into the licensees corrective action program. The inspectors also assessed NRC findings to identify trends.
Annual Follow-up of Selected Issues (IP Section 02.03) (2 Samples 1 Partial)
The inspectors reviewed the licensees implementation of the corrective action program related to the following issues:
(1)
(Partial)
Missing Lateral Support Shim for Reactor Coolant Pump (RCP)-11
- (2) Through-Wall Leak on Unit 1 RCP Seal Injection Lines
- (3) Unit 1 Steam Generator Stop Valve Dump Valve Failed Surveillance
OTHER ACTIVITIES
- TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL
60855.1 - Operation of an Independent Spent Fuel Storage Installation at Operating Plants
Operation of an Independent Spent Fuel Storage Installation at Operating Plants (1 Partial)
(1)
(Partial)
The inspectors closed Unresolved Item 05000315/2018003-002; 05000316/2018003-02, Site Specific Shielding and Barriers for HI-TRAC Transfer Cask Require NRC Approval Prior to Use. The details of this review are documented in the inspection results below. No findings or violations were identified.
INSPECTION RESULTS
Unresolved Item (Closed)
Site Specific Shielding and Barriers for HI-TRAC Transfer Cask Require NRC Approval Prior to Use URI 05000315,05000316/2018003-02 60855.1
Description:
During the 2018 loading campaign, the licensee loaded spent fuel into Holtec Multi-Purpose Canister (MPC) 32 with Holtec International Transfer Cask (HI-TRAC) 125D. The site was using Holtec International Storage Module (HI-STORM) 100 CoC [Certificate of Compliance]
No. 1014, Amendment No. 9, Revision 1 (9R1). During the campaign, the licensee used additional shielding for As Low As Is Reasonably Achievable (ALARA) purposes. The additional shielding was in contact with the upper portions of the HI-TRAC and surrounding, but not in contact, with the HI-TRAC, which could hinder airflow or radiation heat transfer from the HI-TRAC. The licensee identified that the use of the shielding was not bounded by the conditions described in the cask Final Safety Analysis Report (FSAR) and subsequently requested Holtec to perform a site-specific thermal analysis to include the shielding. The site-specific thermal analysis contained inputs that were different than the design basis calculation inputs contained in the FSAR.
The licensee performed a 10 CFR 72.48 screening and evaluation, which concluded that the activity could be implemented without prior NRC approval. Subsequently, the 10 CFR 72.212 report was revised to allow the use of temporary shielding, and the licensee administratively imposed lower building temperatures limits and nuclear fuel assembly heat load limits from those specified in CoC No. 1014, Amendment No. 9R1, as determined in the site-specific thermal analysis. The licensee identified that the use of temporary shielding had the potential to result in CoC No. 1014, Amendment No. 9R1, Appendix B, Design Features, Section 3.9, and Approved Contents, Section 2.4, being non-conservative. Specifically, with the shielding in use, more restrictive requirements than those established in CoC No. 1014, Amendment No. 9R1 were necessary to ensure alignment with the FSAR safety analyses for peak cladding temperature (PCT) limits.
This issue was reviewed by the inspectors and technical specialists in the Division of Spent Fuel Management to determine compliance with Section 3.9 of CoC No. 1014, Amendment No. 9R1, Appendix B; potential non-conservatism of Section 3.9 of CoC No. 1014, Amendment No. 9R1, Appendix B; and compliance with 10 CFR 72.48(c)(1)(ii)(B).
Regarding whether the licensee was compliant with CoC No. 1014, Amendment No. 9R1; Appendix B, Section 3.9, Design Features, stated the following:
Short term operations involving the HI-TRAC transfer cask can be carried out if the reference ambient temperature (three-day average around the cask) is below the Threshold Temperature of 110 degrees F [Fahrenheit] ambient temperature, applicable during HI-TRAC transfer operations inside the 10 CFR Part 50 or 10 CFR Part 52 structural boundary and 90 degrees F outside of it. The determination of the Threshold Temperature compliance shall be made based on the best available thermal data for the site. If the reference ambient temperature exceeds the corresponding Threshold Temperature, then a site-specific analysis shall be performed using the actual heat load and reference ambient temperature equal to the three-day average to ensure that the steady state peak fuel cladding temperature will remain below the 400°C [degrees Celcius] limit.
While the above implied that a site-specific analysis was not necessary when the reference ambient temperature was below the corresponding threshold temperature, it did not preclude a site-specific analysis. Therefore, the licensee performed a site-specific analysis with the use of additional shielding and the administrative limits implemented by the licensee, which were bounded by the limits of Section 3.9 of Holtec CoC No. 1014, Amendment No. 9R1, Appendix B. Therefore, the licensee was compliant with Section 3.9 of Holtec CoC No. 1014, Amendment No. 9R1, Appendix B.
Regarding whether Section 3.9, Design Features, of CoC No. 1014, Amendment No. 9R1, Appendix B, was non-conservative, based on a review of Holtec Report No. HI-2177676, Thermal Evaluation of Shielding on HI-TRAC, which analyzed the transfer cask with temporary shielding in place, the inspectors determined that the use of the temporary shielding rendered the Design Features Section 3.9 and Approved Contents Section 2.4 of CoC No. 1014, Amendment No. 9R1, Appendix B as non-conservative. However, by performing a site-specific thermal analysis and imposing temperature and fuel loading restrictions, the licensee remained compliant with the requirements of CoC No. 1014, Amendment No. 9R1.
Regarding whether the licensee was compliant with 10 CFR 72.48(c)(1)(ii)(B), CNP 72.48 No.
7248-2018-0139-02, Thermal Evaluation of Shielding Package Around the HI-TRAC at D.C.
Cook, provided the 10 CFR 72.48 screening of the proposed activity. The licensee answered No to 10 CFR 72.48 Screening Question E., Does the proposed activity require a change to the ISFSI [Independent Spent Fuel Storage Installation] Technical Specifications or the CoC? The licensee provided the explanation, Calculation package (HI-2177676)provided technical results to demonstrate compliance with CoC No. 1014, Amendment 9, Revision 1.
Based on the determination that the licensee was compliant with Section 3.9 of CoC No.
1014, Amendment No. 9R1, Appendix B, the inspectors did not find any indication that the licensee was not in compliance with 10 CFR 72.48.
Since the licensee was compliant with CoC No. 1014, Amendment No. 9R1, Appendix B and 10 CFR 72.48, the inspectors consider this Unresolved Item closed.
Corrective Action References: AR 2018-4056, AR 2018-6342, and AR 2018-6642 Main Steam Stop Valve Dump Valve Inoperable for Longer than its Technical Specification Allowed Outage Time Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems
Green NCV 05000315/2019003-01 Open/Closed
[H.14] -
Conservative Bias 71152 The inspectors identified a finding of very low safety significance (i.e., Green) and an associated Non-Cited Violation (NCV) of Technical Specification (TS) 3.7.2, Steam Generator Stop Valves (SGVSs), when licensee personnel failed to have four Unit 1 SGSVs and associated actuator trains operable while in Mode 1 and subsequently failed to restore the affected SGSV actuator train and SGSV to an operable status or place Unit 1 in Mode 2 within the time limits specified by the associated TS Limiting Condition for Operation (LCO).
In addition, a NCV of TS 3.0.4, LCO Applicability, was identified because the licensee entered a Mode of applicability without the SGSV actuator train and associated SGSV being operable as required. Specifically, the licensee failed to identify that Unit 1 #2 SGVS Train B Dump Valve MRV-222 was inoperable during a post-maintenance test (PMT) conducted on May 6, 2019; and subsequently entered Mode 1 contrary to TS 3.0.4 and operated for 21 days, contrary to TS 3.7.2.
Description:
During Unit 1 Refueling Outage 29, and while in Mode 2, the licensee adjusted the packing on #2 SGSV Train B Dump Valve 1-MRV-222. This valve was part of the actuation system used to operate the #2 SGSV. On May 6, 2019, following the packing adjustment and prior to a Mode change, the licensee performed portions of the Unit 1 #2 SGSV Train B Dump Valve surveillance test as a post maintenance test. On the first attempt, the valve failed to stroke within the required maximum stroke time of 2 seconds. At that time, the licensee believed that the #2 SGSV Train B Dump Valve operated in a humid environment. To replicate this environment, the licensee wetted the #2 SGSV Train B Dump Valve packing and stem. The valve subsequently passed the surveillance test, the licensee declared the Unit 1 #2 SGSV Train B Dump Valve operable, and on May 9, 2019, transitioned Unit 1 from Mode 2 to Mode 1.
During the next scheduled Unit 1 #2 SGSV Train B Dump Valve surveillance test on May 29, 2019, the valve again failed to stroke within the 2 second stroke time limit. The licensee performed additional investigation and identified that the valve packing had hardened and required replacement. The licensee also identified that the environment that was assumed to exist during the previous troubleshooting effort had been incorrect and that, in fact, the #2 SGSV Train B Dump Valve operated in a non-humid (dry) environment, and therefore the packing was not wet during operation. The packing was replaced, and following a successful PMT the Unit 1 #2 SGSV Train B Dump Valve was returned to service.
During inspection activities to assess the licensees corrective actions, the inspectors identified that the licensee failed to identify that the Unit 1 #2 SGSV Train B Dump Valve and associated #2 SGSV was inoperable from the time Unit 1 entered Mode 1 on May 9, 2019, until the issue was corrected on May 30, 2019. Additionally, the licensee failed to assess the impact of this issue on operability. Following discussions with licensee staff, AR 2019-8511, Past ODE [Operability Determination Evaluation] Possibly Missed, was generated and an operability assessment was performed. This assessment was completed on September 24, 2019, and concluded that the Unit 1 #2 SGSV Train B Dump Valve and associated #2 SGSV was inoperable beginning with the transition to Mode 1 on May 9, 2019, until the valve packing was replaced on May 30, 2019.
Corrective Actions: The licensee performed a past operability assessment under AR 2019-8511. The deficient condition was corrected previously under AR 2019-5615 on May 30, 2019.
Corrective Action References: AR 2019-5615
Performance Assessment:
Performance Deficiency: The inspectors determined that the licensees failure to identify that the Unit 1 #2 SGSV Train B Dump Valve was inoperable during a PMT was a performance deficiency. Specifically, the PMT performed by the licensee created more favorable conditions for valve operation than what existed in the actual operating environment. As a result, the licensee failed to identify that the Unit 1 #2 SGSV Train B Dump Valve and associated #2 SGSV was inoperable.
Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Equipment Performance attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the finding resulted in one train of SGSV actuators being inoperable, causing a delay in the opening of the #2 SGSV and rendering the #2 SGSV also inoperable.
Significance: The inspectors assessed the significance of the finding using Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The inspectors answered Yes to Question A.2 in Exhibit 2 because the Unit 1 #2 SGSV Train B Dump Valve was inoperable for 21 days, which was greater than the TS 3.7.2 Allowed Outage Time of 7 days.
Therefore, a Detailed Risk Evaluation (DRE) was performed using Inspection Manual Chapter (IMC) 0609, Appendix A. The inspectors performed a bounding analysis by failing the Unit 1
- 2 SGSV Train B Dump Valve for 21 days and determined the delta core damage frequency (CDF) was 4.7E-9. As a result, the finding was determined to be of very low safety significance (i.e., Green).
Cross-Cutting Aspect: H.14 - Conservative Bias: Individuals use decision making-practices that emphasize prudent choices over those that are simply allowable. A proposed action is determined to be safe in order to proceed, rather than unsafe in order to stop. Specifically, when troubleshooting the Unit 1 #2 SGSV Train B Dump Valve after its failure on May 6, 2019, the licensee failed to validate the assumptions about the environment in which the valve operated. This caused the licensee to perform an inadequate PMT and ultimately fail to restore the valve to an operable status.
Enforcement:
Violation: Technical Specification 3.7.2, Steam Generator Stop Valves (SGSVs), required that in Mode 1 all four SGSVs and their associated actuator trains be operable. Technical Specification 3.7.2.A required that with one SGSV actuator train inoperable, that the SGSV actuator train be restored to an operable status within 7 days. Technical Specification 3.7.2.E required that if the required action and completion time of Technical Specification 3.7.2.A is not met, to declare each affected SGSV inoperable. Technical Specification 3.7.2.F, Steam Generator Stop Valves (SGSVs), required that with one SGSV inoperable in Mode 1 that the SGSV be restored to an operable status within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />. Technical Specification 3.7.2.G required that if the required action and associated completion time of Technical Specification 3.7.2.F is not met the Unit be placed in Mode 2 within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />.
Technical Specification 3.0.4 required that when a Limiting Condition for Operation is not met, that entry into a Mode applicable to a technical specification shall only be made when, a) the associated actions to be entered permit continued operation in the Mode in the applicability for an unlimited period of time, or b) after the performance of a risk assessment and the establishment of risk management actions, or c) when an allowance is stated in the individual value, parameter, or other specification.
Contrary to the above, on May 9, 2019, with Unit 1 in Mode 1 and with the #2 SGSV Train B Dump Valve, which was a part of the #2 SGSV actuator train, inoperable, the licensee failed to restore the inoperable #2 SGSV actuator train to an operable status within 7 days and failed to declare the associated #2 SGSV inoperable. Also, on May 9, 2019, with Unit 1 in Mode 1 and with the #2 SGSV inoperable, the licensee failed to restore the #2 SGSV to an operable status within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> as required by Technical Specification 3.7.2.F, and failed to place Unit 1 in Mode 2 within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> as required by Technical Specification 3.7.2.G. In addition, prior to entering Mode 1 from Mode 2 on May 9, 2019, with an inoperable SGSV and associated Limiting Condition for Operation 3.7.2.G that did not permit continued operation for an unlimited period of time and did not provide an allowance as stated in an individual value, parameter, or other specification, the licensee failed to perform a risk assessment and establish risk management actions as required by Technical Specification 3.0.4.
Enforcement Action: This violation is being treated as an non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
- On October 15, 2019, the inspectors presented the integrated inspection results to Mr. J. Gebbie, Senior VP and Chief Nuclear Officer, and other members of the licensee staff.
- On August 8, 2019, the inspectors presented the Radioactive Material Processing/Transportation and RCS Specific Activity Performance Indicator inspection results to Mr. S. Lies, Site Vice President, and other members of the licensee staff.
DOCUMENTS REVIEWED
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
71111.04Q Corrective Action
Documents
2018-0075
U1 CD EDG Tripped Due to Air System Issues
01/02/2018
2018-0242
DG1CD Tripped on Overspeed During a Start
01/08/2018
2018-6841
Unit 1 CD EDG Not Synchronizing to T11D Bus
07/02/2018
2018-6917
Potential Commonality in Recent Repeat Events
07/05/2018
2018-9194
Unit 2 PAC Trip
09/27/2018
Drawings
1-OP-5151D-72
Flow Diagram Emergency Diesel Generator CD Unit 1
OP-1-5113A-9
Flow Diagram Essential Service Water
OP-1-5143-80
Flow Diagram Emergency Core Cooling (RHR) Unit No. 1
OP-1-5148C-30
Flow Diagram Diesel Generator Area & Electric Switchgear
Room Heating & Ventilation System Unit 1
OP-1-5151A-50
Flow Diagram Emergency Diesel Generator AB Unit 1
OP-1-5151C-58
Flow Diagram Emergency Diesel Generator CD Unit 1
OP-1-98013-42
Diesel Generator 1AB and Auxiliaries Elementary Diagram
OP-1-98014-40
Diesel Generator 1CD and Auxiliaries Elementary Diagram
OP-1-98016-41
Diesel Generator 1AB Miscellaneous Auxiliaries Elementary
Diagram
OP-1-98017-46
Diesel Generator 1CD Miscellaneous Auxiliaries Elementary
Diagram
OP-2-5143-75
Flow Diagram Emergency Core Cooling (RHR) Unit No. 2
OP-5151B-61
Flow Diagram Emergency Diesel Generator AB Unit #1
Procedures
1-OHP-4012-032-
008CD
Operating DG1CD Subsystems
1-OHP-4021-008-
2
Placing Emergency Core Cooling System in Standby
Readiness
1-OHP-4021-017-
001
Operation of the Residual Heat Removal System
1-OHP-4021-032-
008AB
Operation DG1AB Subsystems
1-OHP-4021-032-
008B
Operating DG1AB Subsystems
1-OHP-4030-156-
017E
East Motor Driven Auxiliary Feedwater System Test
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
2-OHP-4021-008-
Placing Emergency Core Cooling System in Standby
Readiness
2-OHP-4021-032-
008CD
Operating DG2CD Subsystems - DG2CD Starting Air
System Valves
2-OHP-4021-07-
001
Operation of the Residual Heat Removal System
2-OHP-4030-256-
017T
Turbine Driven Auxiliary Feedwater System Test
Work Orders
55501397
MTRI, 2-PPS-1, Calibrate/Replace as Necessary
71111.05Q Drawings
2-5972
Fire Hazards Analysis Plan Below Basement Units 1 and 2
2-5974
Fire Hazard Analysis Mezzanine Floor El. 609 Units 1 & 2
Fire Plans
Fire Pre-Plans Volume 1
Fire Zone 18
CD Diesel Generator Room, Unit 2 Elevation 587
Fire Zone 40A
kV AB Switchgear Room, Unit 1 Elevation 609-0
Fire Zone 47A
4kV AB Switchgear Room, Unit 2 Elevation 609-0
Calculations
MD-12-Flood-
008-N
Flooding Due to Groundwater Level Increase, Cook Nuclear
Plant Flood Hazard Re-Evaluation
PRA-Flood-002
Internal Flooding Impact on Plant Power Distribution
PRA-Flood-004
Internal Flooding - Qualitative Screening Analysis
PRA-Flood-008
Flood Sources and Associated Flood Mechanisms
PRA-Flood-008
Appendix F
Rupture Flow Rates of Flood Sources
SD-061206-001
Flooding Evaluation Report for D.C. Cook Nuclear Power
Plant
Corrective Action
Documents
GT-2015-5625-23 Inspection Frequency for Interim Flood Measures
08/12/2015
Drawings
OP-1-5123A
Station Drainage - Auxiliary Building, Unit 1
OP-12-5123
Station Drainage Auxiliary Building
Procedures
1-OHP-4022
ESW System/Rupture
2-EHP-4075-
TCA-001
Operator Time Critical Actions
2-OHP-4027-
FSG-1501
Flooding Response Deployment
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Drawings
OP-1-5114-152
Flow Diagram Non-Essential Service Water Unit No. 1
OP-2-5114-93
Flow Diagram Non-Essential Service Water Unit No. 2
Procedures
1-OHP-4022
NESW System Loss/Rupture
2-OHP-4021-028-
018
Operation of the Containment Chilled Water System,
Figure 1, System Drawings
71111.11Q Miscellaneous
RQ-C-4431
Secondary Side Break & Pressurized Thermal Shock
Analysis
Pipe Failures in High Energy Systems Due to Erosion
Corrosion
04/02/1987
Corrective Action
Documents
2019-5615-1
1-MRV-222 Failed Surveillance
05/29/2019
Miscellaneous
Two-year Unavailability Report for the Supplemental Diesel
Generator (SDG) System; SSC 12-SDG
09/25/2019
Calculations
DC-D-01-CS-4
Piping and Pipe Support Analysis of CS and RC System for
EBASCO Walkdown Package Nos. CS-11 and RC-09
Corrective Action
Documents
2018-6093
Increasing Unit 1 CCW Out-Leakage
06/06/2018
2018-6615
Unidentified HELB Break Locations
06/26/2018
2018-7570-01
Operability Determination Evaluation (Unit 1 East CCW Heat
Exchanger Leak)
07/27/2018
2019-5237
Asymmetrical Natural Circulation Cooldown Issue with Low
Decay Heat
05/14/2019
2019-5666
Revise Procedure to Support TRM Update
05/30/2019
2019-7053
Pressurizer Insurge/Outsurge
AR 2019-6882
U2 Ice Bed Temps Above eSOMS Notification Limits
07/15/2019
AR 2019-7919
2-HV-AFX Charcoal D/P Outside of ESOMS Limits
08/19/2019
Drawings
1-CS-780-L1-2
Containment
OP-1-5129
CVCS-Reactor Letdown & Charging
OP-12-5148-63
Flow Diagram Auxiliary Building Ventilation Units 1 & 2
Engineering
Changes
0000055754
Install Mechanical Jumper to Connect the Essential Service
Water System to the Component Cooling Water System in
Either Unit to Provide a Source of Makeup Water to the
CCW System
Miscellaneous
FHA Exhaust Fan Charcoal Differential Pressure
08/23/2019
Temporary
Design, Install Mechanical Jumper to Connect the Essential
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Modification 12-
TM-15-49
Service Water System to the Component Cooling Water
System in Either Unit to Provide a Source of Makeup Water
to the CCW System
Rupture of a Steam Pipe
Evaluation of the Effects of Insurge/Outsurge Out-of-Limit
Transients on the Integrity of the Pressurizer Program
MUHP-5063 Summary Report
Procedures
2-OHP-4021-
016-003
Component Cooling Water System Operation
2-OHP-5030-
016-001
Supply ESW to CCW for Makeup Using Temporary
Modification
Work Orders
55504921-01
2-HV-AFX, Auxiliary Building Ventilation Fuel Handling
Area Exhaust Filter Unit, Replace Charcoal Bed
08/23/2017
55504921-02
2-HV-AFX, Auxiliary Building Ventilation Fuel Handling
Area Exhaust Filter Unit, Perform Test After Charcoal
Replacement
08/28/2017
Procedures
OHI-4016
Conduct of Operations: Guidelines
Corrective Action
Documents
2019-8353
Failed PMT 55533608-05, U1 CD Diesel has a Slight Leak
on the 1-R Jacket Water Outlet
08/30/2019
AR-2019-8528
Unit 1 East CCW Pump Surveillance was Aborted Due to #3
09/06/2019
Engineering
Evaluations
DIT-B-03787-01
Restoration of Component Cooling Water Flow to Unit 1
Reactor Coolant Pump #3 Motor Bearing Cooler
09/10/2019
Miscellaneous
Clearance Order
241552
2-IMO-312 Actuator
Procedures
1-OHP-4030-116-
20E
East Component Cooling Water Loop Surveillance Test
09/13/2019
1-OHP-4030-132-
27CD
CD Diesel Generator Operability Test (Train A), DG1CD
Fast Speed Start
2-OHP-4030-208-
053A
ECCS Valve Operability Test - Train A
Shipping Records 55518412-11
MTRS, (R2P) U2 Load New Fuel into SFP
Work Orders
55359920-10
OPS: 2-IMO-312, Stroke for PMT Operability
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
55518169-01
MTRS, (R2P) U2 Unload New 17x17 Fuel
55535360-14
MTM, 2-OME-35N Open NESW PP Strainer and Check for
Debris
97/21/2019
55535386-05
2-OME-35S MTM: 2-OME-35S; Open NESW Strainer and
Check for Debris
07/22/2019
WO Task:
55523374 01
1-FMO-231/Perform A-Found Diagnostic
Miscellaneous
Forced Outage Critical Path
07/22/2019
Procedures
PMP-2291-OLR-
001
Technical Specification 3.0.4.b Risk Assessment Review
and Approval Form for Transitioning Modes with an
Intermediate Range Nuclear Instrument Inoperable
Miscellaneous
2019 DC Cook DR1 Drill Manual
07/30/2019
2019 DC Cook
EMPE Manual
DC Cook EMPE Drill
07/16/2019
DR2 Drill
Scenario Manual
Dress Rehearsal 2 (Team 3)
August 13,
2019
2019 Dress Rehearsal #2
Procedures
RMT-2080-TSC-
001
Activation and Operation of the TSC
RMT-2080-TSC-
CHK-001
Site Emergency Director List
RMT-2080-TSC-
CHK-009
PET-Operations Checklist
Calculations
PMP-2030-REC-
001
2016 10CFR61 Scaling Factor Report
11/08/2017
PMP-2030-REC-
001
2017 10CFR61 Scaling Factor Report
10/29/2018
Engineering
Evaluations
Technical 3002 8-
20A Cask
Cask Handling Procedure for USDOT Spec 7A, Type-A
Transportation Cask
05/14/2018
Self-Assessments GT-2018-1675
Self Assessment of the Radwaste Program at DC Cook that
Covers Radwaste Processing, Handling and Transportation
08/30/2018
Shipping Records DCC18-043
Compactible Trash to Energy Solution Bear Creek Facility
for Processing
05/10/2018
DCC18-044
A Box of Contaminated Equipment to Framatome, Inc.
05/16/2018
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
DCC18-059
Mixed Bed Ion Exchange Spent Resin for Processing to
Energy Solution Bear Creek, Oak Ridge,TN
07/24/2018
DCC18-074
Mixed Bed Resin PRC-1M; Class -B Shipment; UN3321;
LSA-II; RQ; Contained in a Shipping Cask Model 8-120B; to
Energy Solution for processing
11/30/2018
DCC19-033
UN2910 Excepted Package Limited Quantity of Steel Drum
for Part 61 Anlysis
04/15/2019
DCC19-038
Shipment of 2 Sea-Vans Containing Contaminated
Equipment to Westinghouse
04/25/2019
DCC19-041
Compacted Contaminated Trash to Unitech Services, TN
05/01/2019
DCC19-053
Sea-van on a Flatbed Trailer Containing a Shipment
Consigned as UN2913, SCOII Fissile Excepted
06/11/2019
71151
Calculations
PMP-7110-PIP-
001
Reactor Oversight Program Performance Indicators and
Monthly Operating Report Data for Reactor Coolant Specific
Activity; Unit 1 and 2
01/01/2018 -
2/31/2018
Corrective Action
Documents
2019-2963
Investigate Reactor Coolant Pump Seal Injection Line Under
Suspicious Boric Acid Deposit
03/22/2019
2019-4341
Failure to Verify Procedure Directed Terminal Points
04/24/2019
2019-4734
Labeling in Unit 1 Lube Oil Tank Room Junction Box
05/03/2019
2019-4895
1-MRV-222 Failed Post Maintenance Test Timing
05/06/2019
2019-5615
1-MRV-222 Failed Surveillance
05/29/2019
2019-8511
Past Operability Determination Possible Missed
09/05/2019
Miscellaneous
Outage Control Center Shift Package
09/30/2019
Indiana Michigan Power 2019 Second Quarter Trend Report
AEP-19-005
Donald C. Cook Nuclear Plant Safety Review Board Meeting
03/04/2019
NOS-19-002
Nuclear Oversight Quarterly Report for October - December
2018
01/21/2019
NOS-19-006
Nuclear Oversight Quarterly Report for January - March
2019
04/23/2019
UCR 2215
UFSAR Change Request, Data Sheet 1 of PMP-2350-SAR-
001, UFSAR Update Process
Procedures
1-IHP-6040-171-
001
Verification of Turbine Support Systems Interlocks
20