IR 05000315/2019003: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
(StriderTol Bot change)
Line 19: Line 19:


=Text=
=Text=
{{#Wiki_filter:ber 21, 2019
{{#Wiki_filter:November 21, 2019


==SUBJECT:==
==SUBJECT:==
Line 40: Line 40:


Sincerely,
Sincerely,
/RA/
/RA/  
Richard Skokowski, Chief Branch 4 Division of Reactor Projects Docket Nos. 05000315; 05000316; and 07200072 License Nos. DPR-58 and DPR-74
 
Richard Skokowski, Chief Branch 4 Division of Reactor Projects  
 
Docket Nos. 05000315; 05000316; and  
 
07200072 License Nos. DPR-58 and DPR-74  


===Enclosure:===
===Enclosure:===
As stated
As stated  


==Inspection Report==
==Inspection Report==
Docket Numbers: 05000315; 05000316 AND 07200072 License Numbers: DPR-58 and DPR-74 Report Numbers: 05000315/2019003; 05000316/2019003 AND 07200072/2019001 Enterprise Identifier: I-2019-003-0068 AND I-2019-001-0144 Licensee: Indiana Michigan Power Company Facility: Donald C. Cook Nuclear Plant, Units 1 and 2 Location: Bridgman, MI Inspection Dates: July 01, 2019 to September 30, 2019 Inspectors: J. Ellegood, Senior Resident Inspector T. Go, Health Physicist P. LaFlamme, Senior Resident Inspector M. Learn, Reactor Engineer J. Mancuso, Resident Inspector J. Rutkowski, Project Engineer Approved By: R. Skokowski, Chief Branch 4 Division of Reactor Projects Enclosure
Docket Numbers:
05000315; 05000316 AND 07200072  
 
License Numbers:
DPR-58 and DPR-74  
 
Report Numbers:
05000315/2019003; 05000316/2019003 AND 07200072/2019001  
 
Enterprise Identifier: I-2019-003-0068 AND I-2019-001-0144  
 
Licensee:
Indiana Michigan Power Company  
 
Facility:
Donald C. Cook Nuclear Plant, Units 1 and 2  
 
Location:
Bridgman, MI  
 
Inspection Dates:
July 01, 2019 to September 30, 2019  
 
Inspectors:
J. Ellegood, Senior Resident Inspector  
 
T. Go, Health Physicist  
 
P. LaFlamme, Senior Resident Inspector  
 
M. Learn, Reactor Engineer  
 
J. Mancuso, Resident Inspector  
 
J. Rutkowski, Project Engineer  
 
Approved By:
R. Skokowski, Chief
Branch 4
Division of Reactor Projects  


=SUMMARY=
=SUMMARY=
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Donald C. Cook Nuclear Plant, Units 1 and 2 in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Donald C. Cook Nuclear Plant, Units 1 and 2 in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.


List of Findings and Violations Main Steam Stop Valve Dump Valve Inoperable for Longer than its Technical Specification Allowed Outage Time Cornerstone           Significance                                 Cross-Cutting     Report Aspect            Section Mitigating           Green                                         [H.14] -          71152 Systems              NCV 05000315/2019003-01                       Conservative Open/Closed                                   Bias The inspectors identified a finding of very low safety significance (i.e., Green) and an associated Non-Cited Violation (NCV) of Technical Specification (TS) 3.7.2, Steam Generator Stop Valves (SGVSs), when licensee personnel failed to have four Unit 1 SGSVs and associated actuator trains operable while in Mode 1 and subsequently failed to restore the affected SGSV actuator train and SGSV to an operable status or place Unit 1 in Mode 2 within the time limits specified by the associated TS Limiting Condition for Operation (LCO). In addition, a NCV of TS 3.0.4, LCO Applicability, was identified because the licensee entered a Mode of applicability without the SGSV actuator train and associated SGSV being operable as required. Specifically, the licensee failed to identify that Unit 1 #2 SGVS Train B Dump Valve MRV-222 was inoperable during a post-maintenance test (PMT) conducted on May 6, 2019; and subsequently entered Mode 1 contrary to TS 3.0.4 and operated for 21 days, contrary to TS 3.7.2.
===List of Findings and Violations===
Main Steam Stop Valve Dump Valve Inoperable for Longer than its Technical Specification Allowed Outage Time Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000315/2019003-01 Open/Closed  
[H.14] -
Conservative Bias 71152 The inspectors identified a finding of very low safety significance (i.e., Green) and an associated Non-Cited Violation (NCV) of Technical Specification (TS) 3.7.2, Steam Generator Stop Valves (SGVSs), when licensee personnel failed to have four Unit 1 SGSVs and associated actuator trains operable while in Mode 1 and subsequently failed to restore the affected SGSV actuator train and SGSV to an operable status or place Unit 1 in Mode 2 within the time limits specified by the associated TS Limiting Condition for Operation (LCO). In addition, a NCV of TS 3.0.4, LCO Applicability, was identified because the licensee entered a Mode of applicability without the SGSV actuator train and associated SGSV being operable as required. Specifically, the licensee failed to identify that Unit 1 #2 SGVS Train B Dump Valve MRV-222 was inoperable during a post-maintenance test (PMT) conducted on May 6, 2019; and subsequently entered Mode 1 contrary to TS 3.0.4 and operated for 21 days, contrary to TS 3.7.2.


Additional Tracking Items Type       Issue Number                 Title                             Report Section Status URI       05000315,05000316/20         Site Specific Shielding and       60855.1        Closed 18003-02                    Barriers for HI-TRAC Transfer Cask Require NRC Approval Prior to Use
===Additional Tracking Items===
Type Issue Number Title Report Section Status URI 05000315,05000316/20 18003-02 Site Specific Shielding and Barriers for HI-TRAC Transfer Cask Require NRC Approval Prior to Use 60855.1 Closed


=PLANT STATUS=
=PLANT STATUS=
Line 70: Line 118:


==REACTOR SAFETY==
==REACTOR SAFETY==
 
==71111.01 - Adverse Weather Protection==
==71111.01 - Adverse Weather Protection External Flooding Sample (IP Section 03.04)==
===External Flooding Sample (IP Section 03.04) (1 Sample)===
{{IP sample|IP=IP 71111.01|count=1}}
: (1) The inspectors evaluated the licensee's readiness to cope with external flooding for the following area:
: (1) The inspectors evaluated the licensee's readiness to cope with external flooding for the following area:
* Screen House
* Screen House


==71111.04Q - Equipment Alignment Partial Walkdown Sample (IP Section 03.01)==
==71111.04Q - Equipment Alignment==
{{IP sample|IP=IP 71111.04Q|count=5}}
===Partial Walkdown Sample (IP Section 03.01) (5 Samples)===
 
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
: (1) Unit 1 Emergency Diesel Generator (EDG) AB and Associated Support Systems on July 8, 2019
: (1) Unit 1 Emergency Diesel Generator (EDG) AB and Associated Support Systems on July 8, 2019
Line 86: Line 132:
: (5) Unit 2 CD EDG on August 21, 2019
: (5) Unit 2 CD EDG on August 21, 2019


==71111.04S - Equipment Alignment Complete Walkdown Sample (IP Section 03.02)==
==71111.04S - Equipment Alignment==
{{IP sample|IP=IP 71111.04S|count=1}}
===Complete Walkdown Sample (IP Section 03.02) (1 Sample)===
: (1) The inspectors evaluated system configurations during a complete walkdown of the Unit 1 Qualified Offsite Power Lines on September 23, 2019
: (1) The inspectors evaluated system configurations during a complete walkdown of the Unit 1 Qualified Offsite Power Lines on September 23, 2019


==71111.05Q - Fire Protection Quarterly Inspection (IP Section 03.01)==
==71111.05Q - Fire Protection==
{{IP sample|IP=IP 71111.05Q|count=4}}
===Quarterly Inspection (IP Section 03.01) (4 Samples)===
 
The inspectors evaluated fire protection program implementation in the following selected areas:
The inspectors evaluated fire protection program implementation in the following selected areas:
: (1) U2 CD EDG on July 7, 2019
: (1) U2 CD EDG on July 7, 2019
Line 99: Line 144:
: (4) U2 4 Kilovolt (kV) Switchgear Rooms AB and CD on July 11, 2019
: (4) U2 4 Kilovolt (kV) Switchgear Rooms AB and CD on July 11, 2019


==71111.06 - Flood Protection Measures Inspection Activities - Internal Flooding (IP Section 02.02a.)==
==71111.06 - Flood Protection Measures==
{{IP sample|IP=IP 71111.06|count=1}}
===Inspection Activities - Internal Flooding (IP Section 02.02a.) (1 Sample)===
 
The inspectors evaluated internal flooding mitigation protection in the:
The inspectors evaluated internal flooding mitigation protection in the:
: (1) Auxiliary Building, Elevations 573' and 587'
: (1) Auxiliary Building, Elevations 573' and 587'


==71111.07A - Heat Sink Performance Annual Review (IP Section 02.01)==
==71111.07A - Heat Sink Performance==
{{IP sample|IP=IP 71111.07A|count=1}}
===Annual Review (IP Section 02.01) (1 Sample)===
 
The inspectors evaluated readiness and performance of:
The inspectors evaluated readiness and performance of:
: (1) Unit 2 Non-Essential Service Water (NESW)
: (1) Unit 2 Non-Essential Service Water (NESW)


==71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01)==
==71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance==
{{IP sample|IP=IP 71111.11Q|count=1}}
Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)
: (1) The inspectors observed and evaluated licensed operator performance in the Control Room during a plant shutdown for a maintenance outage on July 21, 2019 Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)
: (1) The inspectors observed and evaluated licensed operator performance in the Control Room during a plant shutdown for a maintenance outage on July 21, 2019  
 
===Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)===
: (1) The inspectors observed and evaluated licensed operator requalification training in the Unit 2 Simulator on September 12, 2019
: (1) The inspectors observed and evaluated licensed operator requalification training in the Unit 2 Simulator on September 12, 2019


==71111.12 - Maintenance Effectiveness Routine Maintenance Effectiveness Inspection (IP Section 02.01)==
==71111.12 - Maintenance Effectiveness==
{{IP sample|IP=IP 71111.12|count=3}}
===Routine Maintenance Effectiveness Inspection (IP Section 02.01) (3 Samples)===
 
The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:
The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:
: (1) Unit 1 Auxiliary Feedwater (AFW)
: (1) Unit 1 Auxiliary Feedwater (AFW)
Line 124: Line 168:
: (3) Supplemental Emergency Diesel Generators (EDGs)
: (3) Supplemental Emergency Diesel Generators (EDGs)


==71111.13 - Maintenance Risk Assessments and Emergent Work Control Risk Assessment and Management Sample (IP Section 03.01)==
==71111.13 - Maintenance Risk Assessments and Emergent Work Control==
{{IP sample|IP=IP 71111.13|count=2}}
===Risk Assessment and Management Sample (IP Section 03.01) (2 Samples)===
 
The inspectors evaluated the risk assessments for the following planned and emergent work activities:
The inspectors evaluated the risk assessments for the following planned and emergent work activities:
: (1) Elevated Risk due to unplanned Unit 1 AB EDG inoperability on June 17, 2019
: (1) Elevated Risk due to unplanned Unit 1 AB EDG inoperability on June 17, 2019
: (2) Elevated Risk associated with the loss of Unit 2 NESW from July 21 through July 24, 2019
: (2) Elevated Risk associated with the loss of Unit 2 NESW from July 21 through July 24, 2019


==71111.15 - Operability Determinations and Functionality Assessments Operability Determination or Functionality Assessment (IP Section 02.02)==
==71111.15 - Operability Determinations and Functionality Assessments==
{{IP sample|IP=IP 71111.15|count=5}}
===Operability Determination or Functionality Assessment (IP Section 02.02) (5 Samples)===
 
The inspectors evaluated the following operability determinations and functionality assessments:
The inspectors evaluated the following operability determinations and functionality assessments:
: (1) AR 2015-5237, Asymmetric Natural Circulation Cooldown with Low Decay Heat
: (1) AR 2015-5237, Asymmetric Natural Circulation Cooldown with Low Decay Heat
Line 141: Line 183:
: (5) Step Change in Differential Pressure (D/P) Across Auxiliary Fuel Handling Area Exhaust Filter
: (5) Step Change in Differential Pressure (D/P) Across Auxiliary Fuel Handling Area Exhaust Filter


==71111.19 - Post-Maintenance Testing Post-Maintenance Test Sample (IP Section 03.01)==
==71111.19 - Post-Maintenance Testing==
{{IP sample|IP=IP 71111.19|count=6}}
===Post-Maintenance Test Sample (IP Section 03.01) (6 Samples)===
 
The inspectors evaluated the following post maintenance tests:
The inspectors evaluated the following post maintenance tests:
: (1) Mechanism-Operated Contact Switch Adjustment for Unit 1 AB EDG to 4kV Bus Supply Breaker; Work Order (WO) 55535235
: (1) Mechanism-Operated Contact Switch Adjustment for Unit 1 AB EDG to 4kV Bus Supply Breaker; Work Order (WO) 55535235
Line 150: Line 191:
: (4) Unit 1 CD EDG, on August 29, 2019, following planned maintenance
: (4) Unit 1 CD EDG, on August 29, 2019, following planned maintenance
: (5) Unit 1 TDAFW System on September 3, 2019, following planned maintenance
: (5) Unit 1 TDAFW System on September 3, 2019, following planned maintenance
: (6) Unit 1 East Component Cooling Water (CCW) Check Valve Flow Test following RCP
: (6) Unit 1 East Component Cooling Water (CCW) Check Valve Flow Test following RCP  
          #3 Lower Bearing CCW Throttle Valve Adjustment on September 13, 2019
#3 Lower Bearing CCW Throttle Valve Adjustment on September 13, 2019


==71111.20 - Refueling and Other Outage Activities Refueling/Other Outage Sample (IP Section 03.01)==
==71111.20 - Refueling and Other Outage Activities==
{{IP sample|IP=IP 71111.20|count=1}}
===Refueling/Other Outage Sample (IP Section 03.01) (1 Sample)===
: (1) The inspectors evaluated a Unit 2 maintenance outage from July 21 through July 25, 2019, which resulted from accumulated debris in the NESW strainers
: (1) The inspectors evaluated a Unit 2 maintenance outage from July 21 through July 25, 2019, which resulted from accumulated debris in the NESW strainers


==71111.22 - Surveillance Testing The inspectors evaluated the following surveillance test: Surveillance Tests (other) (IP Section 03.01)==
==71111.22 - Surveillance Testing==
The inspectors evaluated the following surveillance test:  
 
===Surveillance Tests (other) (IP Section 03.01)===
{{IP sample|IP=IP 71111.22|count=1}}
{{IP sample|IP=IP 71111.22|count=1}}
: (1) Unit 2 New Fuel Receipt Inspections; WO 55518169 and WO 55518412
: (1) Unit 2 New Fuel Receipt Inspections; WO 55518169 and WO 55518412
==71114.06 - Drill Evaluation Select Emergency Preparedness Drills and/or Training for Observation (IP Section 03.01)==
{{IP sample|IP=IP 71114.06|count=1}}
: (1) Emergency Preparedness Drill on July 16, 2019


===Drill/Training Evolution Observation (IP Section 03.02)===
==71114.06 - Drill Evaluation==
{{IP sample|IP=IP 71114.06|count=1}}
Select Emergency Preparedness Drills and/or Training for Observation (IP Section 03.01) (1 Sample)
: (1) Emergency Preparedness Drill on July 16, 2019


===Drill/Training Evolution Observation (IP Section 03.02) (1 Sample)===
The inspectors evaluated:
The inspectors evaluated:
: (1) Licensed Operator Requalification Training (LORT) with Drill Exercise Performance (DEP) on September 10,
: (1) Licensed Operator Requalification Training (LORT) with Drill Exercise Performance (DEP) on September 10,


==RADIATION SAFETY==
==RADIATION SAFETY==
==71124.08 - Radioactive Solid Waste Processing and Radioactive Material Handling, Storage,==
and Transportation


==71124.08 - Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and Transportation Radioactive Material Storage (IP Section 02.01)==
===Radioactive Material Storage (IP Section 02.01)===
{{IP sample|IP=IP 71124.08|count=1}}
{{IP sample|IP=IP 71124.08|count=1}}


Line 181: Line 226:
* South Boric-Acid Evaporator Room 587
* South Boric-Acid Evaporator Room 587
* Radioactive Material Building and Contaminated Equipment Storage Area (CESA) Building where Dry Active Waste (DAW) Containers were Stored
* Radioactive Material Building and Contaminated Equipment Storage Area (CESA) Building where Dry Active Waste (DAW) Containers were Stored
* Mausoleum Storage Area and CESA Contains Contaminated Equipment Stored in Sea-Lands The inspectors performed a container check (e.g., swelling, leakage and deformation)on the following containers:
* Mausoleum Storage Area and CESA Contains Contaminated Equipment Stored in Sea-Lands  
 
The inspectors performed a container check (e.g., swelling, leakage and deformation)on the following containers:
* DAW Container No. 321; Air Compressors; dated February 19, 2013
* DAW Container No. 321; Air Compressors; dated February 19, 2013
* DAW Container No. 314; Stinger Whip Welding Equipment; dated July 27, 2017
* DAW Container No. 314; Stinger Whip Welding Equipment; dated July 27, 2017
Line 189: Line 236:
* DAW Container No. 324; Power Packs and Electrical Transformers; dated March 14, 2016
* DAW Container No. 324; Power Packs and Electrical Transformers; dated March 14, 2016
* DAW Container No. 226; Specimen Tools/Bolts for CRD Tools; dated April 28, 2019
* DAW Container No. 226; Specimen Tools/Bolts for CRD Tools; dated April 28, 2019
* DAW Container No. 237; CRDM [Control Rod Drive Mechanism] Equipment Radioactive Waste System Walkdown (IP Section 02.02) (1 Sample)
* DAW Container No. 237; CRDM [Control Rod Drive Mechanism] Equipment  
 
===Radioactive Waste System Walkdown (IP Section 02.02) (1 Sample)===
The inspectors evaluated the following radioactive waste processing systems during plant walkdowns:
The inspectors evaluated the following radioactive waste processing systems during plant walkdowns:
: (1) Liquid or Solid Radioactive Waste Processing Systems
: (1) Liquid or Solid Radioactive Waste Processing Systems
Line 195: Line 244:
* Energy Solution Liquid System; Radioactive Waste Water Demineralizer System
* Energy Solution Liquid System; Radioactive Waste Water Demineralizer System
* Spent Resin Storage Tank Resin Transfer System
* Spent Resin Storage Tank Resin Transfer System
* DAW Trash Loading Located in the Auxiliary Building Radioactive Waste Resin and/or Sludge Discharges Processes
* DAW Trash Loading Located in the Auxiliary Building  
 
Radioactive Waste Resin and/or Sludge Discharges Processes
* Energy Solutions Liquid System; Radioactive Waste Water Demineralizer System
* Energy Solutions Liquid System; Radioactive Waste Water Demineralizer System
* Spent Resin Storage Tank Resin Transfer System Waste Characterization and Classification (IP Section 02.03) (1 Sample)
* Spent Resin Storage Tank Resin Transfer System  
 
===Waste Characterization and Classification (IP Section 02.03) (1 Sample)===
The inspectors evaluated the radioactive waste characterization and classification for the following waste streams:
The inspectors evaluated the radioactive waste characterization and classification for the following waste streams:
: (1) Shipping Cask Containing Spent Resin to Bear Creek, TN; Low Specific Activity (LSA-II)
: (1) Shipping Cask Containing Spent Resin to Bear Creek, TN; Low Specific Activity (LSA-II)
Contaminated Equipment RAM [Radioactive Material] Shipment to Energy Solution Services as Surface Contaminated Objects (SCO-II)
Contaminated Equipment RAM [Radioactive Material] Shipment to Energy Solution Services as Surface Contaminated Objects (SCO-II)
Sample Shipment of 8 Samples to be Analyzed to GEL Laboratory as a Limited Quantity Material
Sample Shipment of 8 Samples to be Analyzed to GEL Laboratory as a Limited Quantity Material  


===Shipment Preparation (IP Section 02.04) (1 Sample)===
===Shipment Preparation (IP Section 02.04) (1 Sample)===
The inspectors evaluated the following radioactive material shipment preparation processes:
The inspectors evaluated the following radioactive material shipment preparation processes:
: (1) DCC18-053; UN3321, RAM LSA-II; Fissile Excepted; 7, RQ-1; Spent Resin Mixed Bed Ion Exchange Media to Bear Creek, TN; dated July 12, 2018 DCC18-074; UN3321, RAM LSA-II; Fissile Excepted; 7, RQ-1; Spent Resin Mixed Bed Ion Exchange Media to Bear Creek, TN; dated December 5, 2018 DCC19-053; UN2913, RAM SCO-II; Fissile Excepted; 7, RQ-1; Contaminated Equipment Contained in a Metal Box to Energy Solution Services, Memphis, TN; dated June 11, 2019
: (1) DCC18-053; UN3321, RAM LSA-II; Fissile Excepted; 7, RQ-1; Spent Resin Mixed Bed Ion Exchange Media to Bear Creek, TN; dated July 12, 2018 DCC18-074; UN3321, RAM LSA-II; Fissile Excepted; 7, RQ-1; Spent Resin Mixed Bed Ion Exchange Media to Bear Creek, TN; dated December 5, 2018 DCC19-053; UN2913, RAM SCO-II; Fissile Excepted; 7, RQ-1; Contaminated Equipment Contained in a Metal Box to Energy Solution Services, Memphis, TN; dated June 11, 2019  


===Shipping Records (IP Section 02.05) (1 Sample)===
===Shipping Records (IP Section 02.05) (1 Sample)===
Line 212: Line 265:


==OTHER ACTIVITIES - BASELINE==
==OTHER ACTIVITIES - BASELINE==
===71151 - Performance Indicator Verification


===71151 - Performance Indicator Verification The inspectors verified licensee performance indicators submittals listed below:
The inspectors verified licensee performance indicators submittals listed below:  
BI01: Reactor Coolant System (RCS) Specific Activity Sample (IP Section 02.10) ===
 
BI01: Reactor Coolant System (RCS) Specific Activity Sample (IP Section 02.10)===
{{IP sample|IP=IP 71151|count=2}}
{{IP sample|IP=IP 71151|count=2}}
: (1) PMP-7110-PIP-001; Reactor Oversight Program Performance Indicators (PIs) and Monthly Operating Report Data for Reactor Coolant Specific Activity; Unit 1; from January 1, 2018 through December 31, 2018
: (1) PMP-7110-PIP-001; Reactor Oversight Program Performance Indicators (PIs) and Monthly Operating Report Data for Reactor Coolant Specific Activity; Unit 1; from January 1, 2018 through December 31, 2018
: (2) PMP-7110-PIP-001; Reactor Oversight Program PIs and Monthly Operating Report Data for Reactor Coolant Specific Activity; Unit 2; from January 1, 2018 through December 31, 2018
: (2) PMP-7110-PIP-001; Reactor Oversight Program PIs and Monthly Operating Report Data for Reactor Coolant Specific Activity; Unit 2; from January 1, 2018 through December 31, 2018


==71152 - Problem Identification and Resolution Semiannual Trend Review (IP Section 02.02)==
==71152 - Problem Identification and Resolution==
{{IP sample|IP=IP 71152|count=1}}
===Semiannual Trend Review (IP Section 02.02) (1 Sample)===
: (1) The inspectors reviewed licensee Nuclear Oversight reports, Nuclear Safety Review Board (NSRB) reports, and System Health summaries to identify potential adverse trends in documented issues that were not entered into the licensees corrective action program. The inspectors also assessed NRC findings to identify trends.
: (1) The inspectors reviewed licensee Nuclear Oversight reports, Nuclear Safety Review Board (NSRB) reports, and System Health summaries to identify potential adverse trends in documented issues that were not entered into the licensees corrective action program. The inspectors also assessed NRC findings to identify trends.


Annual Follow-up of Selected Issues (IP Section 02.03) (2 Samples 1 Partial)
Annual Follow-up of Selected Issues (IP Section 02.03) (2 Samples 1 Partial)  
The inspectors reviewed the licensees implementation of the corrective action program related to the following issues:
 
  (1)   (Partial)
The inspectors reviewed the licensees implementation of the corrective action program related to the following issues:  
 
(1)  
(Partial)
Missing Lateral Support Shim for Reactor Coolant Pump (RCP)-11
Missing Lateral Support Shim for Reactor Coolant Pump (RCP)-11
: (2) Through-Wall Leak on Unit 1 RCP Seal Injection Lines
: (2) Through-Wall Leak on Unit 1 RCP Seal Injection Lines
Line 231: Line 289:


==OTHER ACTIVITIES==
==OTHER ACTIVITIES==
- TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL 60855.1 - Operation of an Independent Spent Fuel Storage Installation at Operating Plants Operation of an Independent Spent Fuel Storage Installation at Operating Plants (1 Partial)
- TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL  
    (1)     (Partial)
 
60855.1 - Operation of an Independent Spent Fuel Storage Installation at Operating Plants  
 
Operation of an Independent Spent Fuel Storage Installation at Operating Plants (1 Partial)  
 
(1)  
(Partial)
The inspectors closed Unresolved Item 05000315/2018003-002; 05000316/2018003-02, Site Specific Shielding and Barriers for HI-TRAC Transfer Cask Require NRC Approval Prior to Use. The details of this review are documented in the inspection results below. No findings or violations were identified.
The inspectors closed Unresolved Item 05000315/2018003-002; 05000316/2018003-02, Site Specific Shielding and Barriers for HI-TRAC Transfer Cask Require NRC Approval Prior to Use. The details of this review are documented in the inspection results below. No findings or violations were identified.


==INSPECTION RESULTS==
==INSPECTION RESULTS==
Unresolved Item       Site Specific Shielding and Barriers for HI-TRAC Transfer     60855.1 (Closed)              Cask Require NRC Approval Prior to Use URI 05000315,05000316/2018003-02
Unresolved Item (Closed)
Site Specific Shielding and Barriers for HI-TRAC Transfer Cask Require NRC Approval Prior to Use URI 05000315,05000316/2018003-02 60855.1


=====Description:=====
=====Description:=====
Line 265: Line 330:
Since the licensee was compliant with CoC No. 1014, Amendment No. 9R1, Appendix B and 10 CFR 72.48, the inspectors consider this Unresolved Item closed.
Since the licensee was compliant with CoC No. 1014, Amendment No. 9R1, Appendix B and 10 CFR 72.48, the inspectors consider this Unresolved Item closed.


Corrective Action References: AR 2018-4056, AR 2018-6342, and AR 2018-6642 Main Steam Stop Valve Dump Valve Inoperable for Longer than its Technical Specification Allowed Outage Time Cornerstone           Significance                               Cross-Cutting   Report Aspect          Section Mitigating             Green                                       [H.14] -        71152 Systems                NCV 05000315/2019003-01                     Conservative Open/Closed                                 Bias The inspectors identified a finding of very low safety significance (i.e., Green) and an associated Non-Cited Violation (NCV) of Technical Specification (TS) 3.7.2, Steam Generator Stop Valves (SGVSs), when licensee personnel failed to have four Unit 1 SGSVs and associated actuator trains operable while in Mode 1 and subsequently failed to restore the affected SGSV actuator train and SGSV to an operable status or place Unit 1 in Mode 2 within the time limits specified by the associated TS Limiting Condition for Operation (LCO).
Corrective Action References: AR 2018-4056, AR 2018-6342, and AR 2018-6642 Main Steam Stop Valve Dump Valve Inoperable for Longer than its Technical Specification Allowed Outage Time Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems
 
Green NCV 05000315/2019003-01 Open/Closed  
 
[H.14] -
Conservative Bias 71152 The inspectors identified a finding of very low safety significance (i.e., Green) and an associated Non-Cited Violation (NCV) of Technical Specification (TS) 3.7.2, Steam Generator Stop Valves (SGVSs), when licensee personnel failed to have four Unit 1 SGSVs and associated actuator trains operable while in Mode 1 and subsequently failed to restore the affected SGSV actuator train and SGSV to an operable status or place Unit 1 in Mode 2 within the time limits specified by the associated TS Limiting Condition for Operation (LCO).


In addition, a NCV of TS 3.0.4, LCO Applicability, was identified because the licensee entered a Mode of applicability without the SGSV actuator train and associated SGSV being operable as required. Specifically, the licensee failed to identify that Unit 1 #2 SGVS Train B Dump Valve MRV-222 was inoperable during a post-maintenance test (PMT) conducted on May 6, 2019; and subsequently entered Mode 1 contrary to TS 3.0.4 and operated for 21 days, contrary to TS 3.7.2.
In addition, a NCV of TS 3.0.4, LCO Applicability, was identified because the licensee entered a Mode of applicability without the SGSV actuator train and associated SGSV being operable as required. Specifically, the licensee failed to identify that Unit 1 #2 SGVS Train B Dump Valve MRV-222 was inoperable during a post-maintenance test (PMT) conducted on May 6, 2019; and subsequently entered Mode 1 contrary to TS 3.0.4 and operated for 21 days, contrary to TS 3.7.2.
Line 278: Line 348:
Corrective Actions: The licensee performed a past operability assessment under AR 2019-8511. The deficient condition was corrected previously under AR 2019-5615 on May 30, 2019.
Corrective Actions: The licensee performed a past operability assessment under AR 2019-8511. The deficient condition was corrected previously under AR 2019-5615 on May 30, 2019.


Corrective Action References: AR 2019-5615
Corrective Action References: AR 2019-5615  


=====Performance Assessment:=====
=====Performance Assessment:=====
Line 287: Line 357:
Significance: The inspectors assessed the significance of the finding using Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The inspectors answered Yes to Question A.2 in Exhibit 2 because the Unit 1 #2 SGSV Train B Dump Valve was inoperable for 21 days, which was greater than the TS 3.7.2 Allowed Outage Time of 7 days.
Significance: The inspectors assessed the significance of the finding using Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The inspectors answered Yes to Question A.2 in Exhibit 2 because the Unit 1 #2 SGSV Train B Dump Valve was inoperable for 21 days, which was greater than the TS 3.7.2 Allowed Outage Time of 7 days.


Therefore, a Detailed Risk Evaluation (DRE) was performed using Inspection Manual Chapter (IMC) 0609, Appendix A. The inspectors performed a bounding analysis by failing the Unit 1
Therefore, a Detailed Risk Evaluation (DRE) was performed using Inspection Manual Chapter (IMC) 0609, Appendix A. The inspectors performed a bounding analysis by failing the Unit 1  
#2 SGSV Train B Dump Valve for 21 days and determined the delta core damage frequency (CDF) was 4.7E-9. As a result, the finding was determined to be of very low safety significance (i.e., Green).
#2 SGSV Train B Dump Valve for 21 days and determined the delta core damage frequency (CDF) was 4.7E-9. As a result, the finding was determined to be of very low safety significance (i.e., Green).


Line 308: Line 378:
=DOCUMENTS REVIEWED=
=DOCUMENTS REVIEWED=


Inspection Type             Designation     Description or Title                                     Revision or
Inspection
Procedure                                                                                            Date
Procedure
71111.04Q Corrective Action 2018-0075       U1 CD EDG Tripped Due to Air System Issues               01/02/2018
Type
Documents        2018-0242       DG1CD Tripped on Overspeed During a Start                 01/08/2018
Designation
2018-6841       Unit 1 CD EDG Not Synchronizing to T11D Bus               07/02/2018
Description or Title
2018-6917       Potential Commonality in Recent Repeat Events             07/05/2018
Revision or
2018-9194       Unit 2 PAC Trip                                           09/27/2018
Date
Drawings         1-OP-5151D-72   Flow Diagram Emergency Diesel Generator CD Unit 1
71111.04Q Corrective Action
OP-1-5113A-9   Flow Diagram Essential Service Water
Documents
OP-1-5143-80   Flow Diagram Emergency Core Cooling (RHR) Unit No. 1
2018-0075
OP-1-5148C-30   Flow Diagram Diesel Generator Area & Electric Switchgear
U1 CD EDG Tripped Due to Air System Issues
01/02/2018
2018-0242
DG1CD Tripped on Overspeed During a Start
01/08/2018
2018-6841
Unit 1 CD EDG Not Synchronizing to T11D Bus
07/02/2018
2018-6917
Potential Commonality in Recent Repeat Events
07/05/2018
2018-9194
Unit 2 PAC Trip
09/27/2018
Drawings
1-OP-5151D-72
Flow Diagram Emergency Diesel Generator CD Unit 1
OP-1-5113A-9
Flow Diagram Essential Service Water
OP-1-5143-80
Flow Diagram Emergency Core Cooling (RHR) Unit No. 1
OP-1-5148C-30
Flow Diagram Diesel Generator Area & Electric Switchgear
Room Heating & Ventilation System Unit 1
Room Heating & Ventilation System Unit 1
OP-1-5151A-50   Flow Diagram Emergency Diesel Generator AB Unit 1
OP-1-5151A-50
OP-1-5151C-58   Flow Diagram Emergency Diesel Generator CD Unit 1
Flow Diagram Emergency Diesel Generator AB Unit 1
OP-1-98013-42   Diesel Generator 1AB and Auxiliaries Elementary Diagram
OP-1-5151C-58
OP-1-98014-40   Diesel Generator 1CD and Auxiliaries Elementary Diagram
Flow Diagram Emergency Diesel Generator CD Unit 1
OP-1-98016-41   Diesel Generator 1AB Miscellaneous Auxiliaries Elementary
OP-1-98013-42
Diesel Generator 1AB and Auxiliaries Elementary Diagram
OP-1-98014-40
Diesel Generator 1CD and Auxiliaries Elementary Diagram
OP-1-98016-41
Diesel Generator 1AB Miscellaneous Auxiliaries Elementary
Diagram
Diagram
OP-1-98017-46   Diesel Generator 1CD Miscellaneous Auxiliaries Elementary
OP-1-98017-46
Diesel Generator 1CD Miscellaneous Auxiliaries Elementary
Diagram
Diagram
OP-2-5143-75   Flow Diagram Emergency Core Cooling (RHR) Unit No. 2
OP-2-5143-75
OP-5151B-61     Flow Diagram Emergency Diesel Generator AB Unit #1
Flow Diagram Emergency Core Cooling (RHR) Unit No. 2
Procedures       1-OHP-4012-032- Operating DG1CD Subsystems                                37
OP-5151B-61
Flow Diagram Emergency Diesel Generator AB Unit #1
Procedures
1-OHP-4012-032-
008CD
008CD
1-OHP-4021-008- Placing Emergency Core Cooling System in Standby         36
Operating DG1CD Subsystems
2            Readiness
1-OHP-4021-008-
1-OHP-4021-017- Operation of the Residual Heat Removal System            31
2
Placing Emergency Core Cooling System in Standby
Readiness
1-OHP-4021-017-
001
001
1-OHP-4021-032- Operation DG1AB Subsystems                                32
Operation of the Residual Heat Removal System
1-OHP-4021-032-
008AB
008AB
1-OHP-4021-032- Operating DG1AB Subsystems                                30
Operation DG1AB Subsystems
1-OHP-4021-032-
008B
008B
1-OHP-4030-156- East Motor Driven Auxiliary Feedwater System Test        14
Operating DG1AB Subsystems
1-OHP-4030-156-
017E
017E
Inspection Type             Designation     Description or Title                                     Revision or
East Motor Driven Auxiliary Feedwater System Test
Procedure                                                                                              Date
 
2-OHP-4021-008- Placing Emergency Core Cooling System in Standby         36
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
2-OHP-4021-008-
Placing Emergency Core Cooling System in Standby
Readiness
Readiness
2-OHP-4021-032- Operating DG2CD Subsystems - DG2CD Starting Air           32
2-OHP-4021-032-
008CD          System Valves
008CD
2-OHP-4021-07- Operation of the Residual Heat Removal System            27
Operating DG2CD Subsystems - DG2CD Starting Air
System Valves
2-OHP-4021-07-
001
001
2-OHP-4030-256- Turbine Driven Auxiliary Feedwater System Test            31
Operation of the Residual Heat Removal System
2-OHP-4030-256-
017T
017T
Work Orders       55501397       MTRI, 2-PPS-1, Calibrate/Replace as Necessary
Turbine Driven Auxiliary Feedwater System Test
71111.05Q Drawings           12-5972         Fire Hazards Analysis Plan Below Basement Units 1 and 2   5
Work Orders
2-5974         Fire Hazard Analysis Mezzanine Floor El. 609 Units 1 & 2 12
55501397
Fire Plans                       Fire Pre-Plans Volume 1                                   33
MTRI, 2-PPS-1, Calibrate/Replace as Necessary
Fire Zone 18   2 CD Diesel Generator Room, Unit 2 Elevation 587         33
71111.05Q Drawings
Fire Zone 40A   4 kV AB Switchgear Room, Unit 1 Elevation 609-0         33
2-5972
Fire Zone 47A   4kV AB Switchgear Room, Unit 2 Elevation 609-0         33
Fire Hazards Analysis Plan Below Basement Units 1 and 2
71111.06   Calculations     MD-12-Flood-   Flooding Due to Groundwater Level Increase, Cook Nuclear 1
2-5974
008-N          Plant Flood Hazard Re-Evaluation
Fire Hazard Analysis Mezzanine Floor El. 609 Units 1 & 2
PRA-Flood-002   Internal Flooding Impact on Plant Power Distribution     1
Fire Plans
PRA-Flood-004   Internal Flooding - Qualitative Screening Analysis       2
Fire Pre-Plans Volume 1
PRA-Flood-008   Flood Sources and Associated Flood Mechanisms             2
Fire Zone 18
PRA-Flood-008   Rupture Flow Rates of Flood Sources                      2
CD Diesel Generator Room, Unit 2 Elevation 587
Fire Zone 40A
kV AB Switchgear Room, Unit 1 Elevation 609-0
Fire Zone 47A
4kV AB Switchgear Room, Unit 2 Elevation 609-0
71111.06
Calculations
MD-12-Flood-
008-N
Flooding Due to Groundwater Level Increase, Cook Nuclear
Plant Flood Hazard Re-Evaluation
PRA-Flood-002
Internal Flooding Impact on Plant Power Distribution
PRA-Flood-004
Internal Flooding - Qualitative Screening Analysis
PRA-Flood-008
Flood Sources and Associated Flood Mechanisms
PRA-Flood-008
Appendix F
Appendix F
SD-061206-001   Flooding Evaluation Report for D.C. Cook Nuclear Power   3
Rupture Flow Rates of Flood Sources
SD-061206-001
Flooding Evaluation Report for D.C. Cook Nuclear Power
Plant
Plant
Corrective Action GT-2015-5625-23 Inspection Frequency for Interim Flood Measures          08/12/2015
Corrective Action
Documents
Documents
Drawings         OP-1-5123A     Station Drainage - Auxiliary Building, Unit 1             21
GT-2015-5625-23 Inspection Frequency for Interim Flood Measures
OP-12-5123     Station Drainage Auxiliary Building                       14
08/12/2015
Procedures       1-OHP-4022     ESW System/Rupture                                       11
Drawings
2-EHP-4075-   Operator Time Critical Actions                            16
OP-1-5123A
Station Drainage - Auxiliary Building, Unit 1
OP-12-5123
Station Drainage Auxiliary Building
Procedures
1-OHP-4022
ESW System/Rupture
2-EHP-4075-
TCA-001
TCA-001
2-OHP-4027-   Flooding Response Deployment                              1
Operator Time Critical Actions
2-OHP-4027-
FSG-1501
FSG-1501
Inspection Type             Designation     Description or Title                                       Revision or
Flooding Response Deployment
Procedure                                                                                              Date
 
71111.07A Drawings         OP-1-5114-152   Flow Diagram Non-Essential Service Water Unit No. 1
Inspection
OP-2-5114-93   Flow Diagram Non-Essential Service Water Unit No. 2
Procedure
Procedures       1-OHP-4022     NESW System Loss/Rupture                                   14
Type
2-OHP-4021-028- Operation of the Containment Chilled Water System,         44
Designation
018            Figure 1, System Drawings
Description or Title
71111.11Q Miscellaneous     RQ-C-4431       Secondary Side Break & Pressurized Thermal Shock           1
Revision or
Date
71111.07A
Drawings
OP-1-5114-152
Flow Diagram Non-Essential Service Water Unit No. 1
OP-2-5114-93
Flow Diagram Non-Essential Service Water Unit No. 2
Procedures
1-OHP-4022
NESW System Loss/Rupture
2-OHP-4021-028-
018
Operation of the Containment Chilled Water System,
Figure 1, System Drawings
71111.11Q Miscellaneous
RQ-C-4431
Secondary Side Break & Pressurized Thermal Shock
Analysis
Analysis
SOER 87-3       Pipe Failures in High Energy Systems Due to Erosion       04/02/1987
SOER 87-3
Pipe Failures in High Energy Systems Due to Erosion
Corrosion
Corrosion
71111.12   Corrective Action 2019-5615-1    1-MRV-222 Failed Surveillance                              05/29/2019
04/02/1987
71111.12
Corrective Action
Documents
Documents
Miscellaneous                     Two-year Unavailability Report for the Supplemental Diesel 09/25/2019
2019-5615-1
1-MRV-222 Failed Surveillance
05/29/2019
Miscellaneous
Two-year Unavailability Report for the Supplemental Diesel
Generator (SDG) System; SSC 12-SDG
Generator (SDG) System; SSC 12-SDG
71111.15   Calculations     DC-D-01-CS-4   Piping and Pipe Support Analysis of CS and RC System for   02
09/25/2019
71111.15
Calculations
DC-D-01-CS-4
Piping and Pipe Support Analysis of CS and RC System for
EBASCO Walkdown Package Nos. CS-11 and RC-09
EBASCO Walkdown Package Nos. CS-11 and RC-09
Corrective Action 2018-6093       Increasing Unit 1 CCW Out-Leakage                         06/06/2018
Corrective Action
Documents        2018-6615       Unidentified HELB Break Locations                         06/26/2018
Documents
2018-7570-01   Operability Determination Evaluation (Unit 1 East CCW Heat 07/27/2018
2018-6093
Increasing Unit 1 CCW Out-Leakage
06/06/2018
2018-6615
Unidentified HELB Break Locations
06/26/2018
2018-7570-01
Operability Determination Evaluation (Unit 1 East CCW Heat
Exchanger Leak)
Exchanger Leak)
2019-5237       Asymmetrical Natural Circulation Cooldown Issue with Low   05/14/2019
07/27/2018
2019-5237
Asymmetrical Natural Circulation Cooldown Issue with Low
Decay Heat
Decay Heat
2019-5666       Revise Procedure to Support TRM Update                     05/30/2019
05/14/2019
2019-7053       Pressurizer Insurge/Outsurge
2019-5666
AR 2019-6882   U2 Ice Bed Temps Above eSOMS Notification Limits           07/15/2019
Revise Procedure to Support TRM Update
AR 2019-7919   12-HV-AFX Charcoal D/P Outside of ESOMS Limits             08/19/2019
05/30/2019
Drawings         1-CS-780-L1-2   Containment                                               3
2019-7053
OP-1-5129       CVCS-Reactor Letdown & Charging                           68
Pressurizer Insurge/Outsurge
OP-12-5148-63   Flow Diagram Auxiliary Building Ventilation Units 1 & 2   63
AR 2019-6882
Engineering       0000055754     Install Mechanical Jumper to Connect the Essential Service 01
U2 Ice Bed Temps Above eSOMS Notification Limits
Changes                          Water System to the Component Cooling Water System in
07/15/2019
AR 2019-7919
2-HV-AFX Charcoal D/P Outside of ESOMS Limits
08/19/2019
Drawings
1-CS-780-L1-2
Containment
OP-1-5129
CVCS-Reactor Letdown & Charging
OP-12-5148-63
Flow Diagram Auxiliary Building Ventilation Units 1 & 2
Engineering
Changes
0000055754
Install Mechanical Jumper to Connect the Essential Service
Water System to the Component Cooling Water System in
Either Unit to Provide a Source of Makeup Water to the
Either Unit to Provide a Source of Makeup Water to the
CCW System
CCW System
Miscellaneous                     FHA Exhaust Fan Charcoal Differential Pressure             08/23/2019
Miscellaneous
Temporary       Design, Install Mechanical Jumper to Connect the Essential 03
FHA Exhaust Fan Charcoal Differential Pressure
Inspection Type             Designation     Description or Title                                       Revision or
08/23/2019
Procedure                                                                                                Date
Temporary
Modification 12- Service Water System to the Component Cooling Water
Design, Install Mechanical Jumper to Connect the Essential  
TM-15-49        System in Either Unit to Provide a Source of Makeup Water
 
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Modification 12-
TM-15-49
Service Water System to the Component Cooling Water
System in Either Unit to Provide a Source of Makeup Water
to the CCW System
to the CCW System
UFSAR Section   Rupture of a Steam Pipe                                    28
UFSAR Section
14.2.5
14.2.5
WCAP-14717       Evaluation of the Effects of Insurge/Outsurge Out-of-Limit
Rupture of a Steam Pipe
WCAP-14717
Evaluation of the Effects of Insurge/Outsurge Out-of-Limit
Transients on the Integrity of the Pressurizer Program
Transients on the Integrity of the Pressurizer Program
MUHP-5063 Summary Report
MUHP-5063 Summary Report
Procedures       12-OHP-4021-     Component Cooling Water System Operation                  48
Procedures
2-OHP-4021-
016-003
016-003
2-OHP-5030-     Supply ESW to CCW for Makeup Using Temporary               4
Component Cooling Water System Operation
016-001          Modification
2-OHP-5030-
Work Orders       55504921-01     12-HV-AFX, Auxiliary Building Ventilation Fuel Handling   08/23/2017
016-001
Supply ESW to CCW for Makeup Using Temporary
Modification
Work Orders
55504921-01
2-HV-AFX, Auxiliary Building Ventilation Fuel Handling
Area Exhaust Filter Unit, Replace Charcoal Bed
Area Exhaust Filter Unit, Replace Charcoal Bed
55504921-02     12-HV-AFX, Auxiliary Building Ventilation Fuel Handling   08/28/2017
08/23/2017
55504921-02
2-HV-AFX, Auxiliary Building Ventilation Fuel Handling
Area Exhaust Filter Unit, Perform Test After Charcoal
Area Exhaust Filter Unit, Perform Test After Charcoal
Replacement
Replacement
71111.18   Procedures       OHI-4016         Conduct of Operations: Guidelines                         56
08/28/2017
71111.19   Corrective Action 2019-8353       Failed PMT 55533608-05, U1 CD Diesel has a Slight Leak     08/30/2019
71111.18
Documents                          on the 1-R Jacket Water Outlet
Procedures
AR-2019-8528     Unit 1 East CCW Pump Surveillance was Aborted Due to #3   09/06/2019
OHI-4016
Conduct of Operations: Guidelines
71111.19
Corrective Action
Documents
2019-8353
Failed PMT 55533608-05, U1 CD Diesel has a Slight Leak
on the 1-R Jacket Water Outlet
08/30/2019
AR-2019-8528
Unit 1 East CCW Pump Surveillance was Aborted Due to #3
RCP CCW Flows
RCP CCW Flows
Engineering       DIT-B-03787-01   Restoration of Component Cooling Water Flow to Unit 1     09/10/2019
09/06/2019
Evaluations                        Reactor Coolant Pump #3 Motor Bearing Cooler
Engineering
Miscellaneous     Clearance Order 2-IMO-312 Actuator
Evaluations
DIT-B-03787-01
Restoration of Component Cooling Water Flow to Unit 1
Reactor Coolant Pump #3 Motor Bearing Cooler
09/10/2019
Miscellaneous
Clearance Order
241552
241552
Procedures       1-OHP-4030-116- East Component Cooling Water Loop Surveillance Test        09/13/2019
2-IMO-312 Actuator
Procedures
1-OHP-4030-116-
20E
20E
1-OHP-4030-132- CD Diesel Generator Operability Test (Train A), DG1CD     57
East Component Cooling Water Loop Surveillance Test
27CD            Fast Speed Start
09/13/2019
2-OHP-4030-208- ECCS Valve Operability Test - Train A                      35
1-OHP-4030-132-
27CD
CD Diesel Generator Operability Test (Train A), DG1CD
Fast Speed Start
2-OHP-4030-208-
053A
053A
Shipping Records 55518412-11     MTRS, (R2P) U2 Load New Fuel into SFP
ECCS Valve Operability Test - Train A
Work Orders       55359920-10     OPS: 2-IMO-312, Stroke for PMT Operability
Shipping Records 55518412-11
Inspection Type             Designation       Description or Title                                     Revision or
MTRS, (R2P) U2 Load New Fuel into SFP
Procedure                                                                                              Date
Work Orders
55518169-01       MTRS, (R2P) U2 Unload New 17x17 Fuel
55359920-10
55535360-14       MTM, 2-OME-35N Open NESW PP Strainer and Check for       97/21/2019
OPS: 2-IMO-312, Stroke for PMT Operability  
 
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
55518169-01
MTRS, (R2P) U2 Unload New 17x17 Fuel
55535360-14
MTM, 2-OME-35N Open NESW PP Strainer and Check for
Debris
Debris
55535386-05       2-OME-35S MTM: 2-OME-35S; Open NESW Strainer and         07/22/2019
97/21/2019
55535386-05
2-OME-35S MTM: 2-OME-35S; Open NESW Strainer and
Check for Debris
Check for Debris
WO Task:         1-FMO-231/Perform A-Found Diagnostic                  01
07/22/2019
WO Task:
55523374 01
55523374 01
71111.20   Miscellaneous                     Forced Outage Critical Path                             07/22/2019
1-FMO-231/Perform A-Found Diagnostic
Procedures       PMP-2291-OLR-     Technical Specification 3.0.4.b Risk Assessment Review   46
71111.20
001              and Approval Form for Transitioning Modes with an
Miscellaneous
Forced Outage Critical Path
07/22/2019
Procedures
PMP-2291-OLR-
001
Technical Specification 3.0.4.b Risk Assessment Review
and Approval Form for Transitioning Modes with an
Intermediate Range Nuclear Instrument Inoperable
Intermediate Range Nuclear Instrument Inoperable
71114.06   Miscellaneous                     2019 DC Cook DR1 Drill Manual                           07/30/2019
71114.06
2019 DC Cook     DC Cook EMPE Drill                                      07/16/2019
Miscellaneous
2019 DC Cook DR1 Drill Manual
07/30/2019
2019 DC Cook
EMPE Manual
EMPE Manual
DR2 Drill         Dress Rehearsal 2 (Team 3)                               August 13,
DC Cook EMPE Drill
Scenario Manual                                                            2019
07/16/2019
EP-S-19DR2       2019 Dress Rehearsal #2                                 1
DR2 Drill
Procedures       RMT-2080-TSC-     Activation and Operation of the TSC                      27
Scenario Manual
Dress Rehearsal 2 (Team 3)
August 13,
2019
EP-S-19DR2
2019 Dress Rehearsal #2
Procedures
RMT-2080-TSC-
001
001
RMT-2080-TSC-     Site Emergency Director List                            1
Activation and Operation of the TSC
RMT-2080-TSC-
CHK-001
CHK-001
RMT-2080-TSC-     PET-Operations Checklist                                0
Site Emergency Director List
RMT-2080-TSC-
CHK-009
CHK-009
71124.08   Calculations     PMP-2030-REC-     2016 10CFR61 Scaling Factor Report                      11/08/2017
PET-Operations Checklist
71124.08
Calculations
PMP-2030-REC-
001
001
PMP-2030-REC-     2017 10CFR61 Scaling Factor Report                      10/29/2018
2016 10CFR61 Scaling Factor Report
11/08/2017
PMP-2030-REC-
001
001
Engineering     Technical 3002 8- Cask Handling Procedure for USDOT Spec 7A, Type-A       05/14/2018
2017 10CFR61 Scaling Factor Report
Evaluations      120A Cask        Transportation Cask
10/29/2018
Self-Assessments GT-2018-1675     Self Assessment of the Radwaste Program at DC Cook that 08/30/2018
Engineering
Evaluations
Technical 3002 8-
20A Cask
Cask Handling Procedure for USDOT Spec 7A, Type-A
Transportation Cask
05/14/2018
Self-Assessments GT-2018-1675
Self Assessment of the Radwaste Program at DC Cook that
Covers Radwaste Processing, Handling and Transportation
Covers Radwaste Processing, Handling and Transportation
Shipping Records DCC18-043         Compactible Trash to Energy Solution Bear Creek Facility 05/10/2018
08/30/2018
Shipping Records DCC18-043
Compactible Trash to Energy Solution Bear Creek Facility
for Processing
for Processing
DCC18-044         A Box of Contaminated Equipment to Framatome, Inc.       05/16/2018
05/10/2018
Inspection Type             Designation     Description or Title                                       Revision or
DCC18-044
Procedure                                                                                              Date
A Box of Contaminated Equipment to Framatome, Inc.
DCC18-059       Mixed Bed Ion Exchange Spent Resin for Processing to       07/24/2018
05/16/2018  
 
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
DCC18-059
Mixed Bed Ion Exchange Spent Resin for Processing to
Energy Solution Bear Creek, Oak Ridge,TN
Energy Solution Bear Creek, Oak Ridge,TN
DCC18-074       Mixed Bed Resin PRC-1M; Class -B Shipment; UN3321;         11/30/2018
07/24/2018
DCC18-074
Mixed Bed Resin PRC-1M; Class -B Shipment; UN3321;
LSA-II; RQ; Contained in a Shipping Cask Model 8-120B; to
LSA-II; RQ; Contained in a Shipping Cask Model 8-120B; to
Energy Solution for processing
Energy Solution for processing
DCC19-033       UN2910 Excepted Package Limited Quantity of Steel Drum     04/15/2019
11/30/2018
DCC19-033
UN2910 Excepted Package Limited Quantity of Steel Drum
for Part 61 Anlysis
for Part 61 Anlysis
DCC19-038       Shipment of 2 Sea-Vans Containing Contaminated             04/25/2019
04/15/2019
DCC19-038
Shipment of 2 Sea-Vans Containing Contaminated
Equipment to Westinghouse
Equipment to Westinghouse
DCC19-041       Compacted Contaminated Trash to Unitech Services, TN       05/01/2019
04/25/2019
DCC19-053       1 Sea-van on a Flatbed Trailer Containing a Shipment       06/11/2019
DCC19-041
Compacted Contaminated Trash to Unitech Services, TN
05/01/2019
DCC19-053
Sea-van on a Flatbed Trailer Containing a Shipment
Consigned as UN2913, SCOII Fissile Excepted
Consigned as UN2913, SCOII Fissile Excepted
71151     Calculations     PMP-7110-PIP-   Reactor Oversight Program Performance Indicators and       01/01/2018 -
06/11/2019
001            Monthly Operating Report Data for Reactor Coolant Specific 12/31/2018
71151
Calculations
PMP-7110-PIP-
001
Reactor Oversight Program Performance Indicators and
Monthly Operating Report Data for Reactor Coolant Specific
Activity; Unit 1 and 2
Activity; Unit 1 and 2
71152     Corrective Action 2019-2963       Investigate Reactor Coolant Pump Seal Injection Line Under 03/22/2019
01/01/2018 -
Documents                        Suspicious Boric Acid Deposit
2/31/2018
2019-4341       Failure to Verify Procedure Directed Terminal Points       04/24/2019
71152
2019-4734       Labeling in Unit 1 Lube Oil Tank Room Junction Box         05/03/2019
Corrective Action
2019-4895       1-MRV-222 Failed Post Maintenance Test Timing             05/06/2019
Documents
2019-5615       1-MRV-222 Failed Surveillance                             05/29/2019
2019-2963
2019-8511       Past Operability Determination Possible Missed             09/05/2019
Investigate Reactor Coolant Pump Seal Injection Line Under
Miscellaneous                     Outage Control Center Shift Package                       09/30/2019
Suspicious Boric Acid Deposit
03/22/2019
2019-4341
Failure to Verify Procedure Directed Terminal Points
04/24/2019
2019-4734
Labeling in Unit 1 Lube Oil Tank Room Junction Box
05/03/2019
2019-4895
1-MRV-222 Failed Post Maintenance Test Timing
05/06/2019
2019-5615
1-MRV-222 Failed Surveillance
05/29/2019
2019-8511
Past Operability Determination Possible Missed
09/05/2019
Miscellaneous
Outage Control Center Shift Package
09/30/2019
Indiana Michigan Power 2019 Second Quarter Trend Report
Indiana Michigan Power 2019 Second Quarter Trend Report
AEP-19-005     Donald C. Cook Nuclear Plant Safety Review Board Meeting   03/04/2019
AEP-19-005
NOS-19-002     Nuclear Oversight Quarterly Report for October - December 01/21/2019
Donald C. Cook Nuclear Plant Safety Review Board Meeting
03/04/2019
NOS-19-002
Nuclear Oversight Quarterly Report for October - December
2018
2018
NOS-19-006     Nuclear Oversight Quarterly Report for January - March     04/23/2019
01/21/2019
NOS-19-006
Nuclear Oversight Quarterly Report for January - March
2019
2019
UCR 2215       UFSAR Change Request, Data Sheet 1 of PMP-2350-SAR-       0
04/23/2019
UCR 2215
UFSAR Change Request, Data Sheet 1 of PMP-2350-SAR-
001, UFSAR Update Process
001, UFSAR Update Process
Procedures       1-IHP-6040-171- Verification of Turbine Support Systems Interlocks        4
Procedures
1-IHP-6040-171-
001
001
Verification of Turbine Support Systems Interlocks
20
20
}}
}}

Revision as of 08:51, 31 December 2024

Reissue - Donald C. Cook Nuclear Plant, Units 1 and 2 - Integrated Inspection Report 05000315/2019003; 05000316/2019003 and 07200072/2019001
ML19326B800
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 11/21/2019
From: Richard Skokowski
Reactor Projects Region 3 Branch 4
To: Gebbie J
Indiana Michigan Power Co
Shared Package
ML19326B837 List:
References
IR 2019003
Download: ML19326B800 (23)


Text

November 21, 2019

SUBJECT:

REISSUE - DONALD C. COOK NUCLEAR PLANT, UNITS 1 AND 2 -

INTEGRATED INSPECTION REPORT 05000315/2019003; 05000316/2019003 AND 07200072/2019001

Dear Mr. Gebbie:

The NRC identified that the inspection report sent to you dated November 7, 2019 (ML19312A445) inadvertently failed to reference the Independent Spent Fuel Storage Installation Inspection Report number 07200072/2019001. As a result, the NRC is reissuing the report in its entirety with the updated subject. None of these changes affected the technical content of the report.

On September 30, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Donald C. Cook Nuclear Plant, Units 1 and 2. On October 15, 2019, the NRC inspectors discussed the results of this inspection with you and other members of your staff.

The results of this inspection are documented in the enclosed report.

One finding of very low safety significance (Green) is documented in this report. This finding involved a violation of NRC requirements. We are treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violation or significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; the Director, Office of Enforcement; and the NRC Resident Inspector at D.C. Cook.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; and the NRC Resident Inspector at D.C. Cook. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Richard Skokowski, Chief Branch 4 Division of Reactor Projects

Docket Nos. 05000315; 05000316; and

07200072 License Nos. DPR-58 and DPR-74

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000315; 05000316 AND 07200072

License Numbers:

DPR-58 and DPR-74

Report Numbers:

05000315/2019003; 05000316/2019003 AND 07200072/2019001

Enterprise Identifier: I-2019-003-0068 AND I-2019-001-0144

Licensee:

Indiana Michigan Power Company

Facility:

Donald C. Cook Nuclear Plant, Units 1 and 2

Location:

Bridgman, MI

Inspection Dates:

July 01, 2019 to September 30, 2019

Inspectors:

J. Ellegood, Senior Resident Inspector

T. Go, Health Physicist

P. LaFlamme, Senior Resident Inspector

M. Learn, Reactor Engineer

J. Mancuso, Resident Inspector

J. Rutkowski, Project Engineer

Approved By:

R. Skokowski, Chief

Branch 4

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Donald C. Cook Nuclear Plant, Units 1 and 2 in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Main Steam Stop Valve Dump Valve Inoperable for Longer than its Technical Specification Allowed Outage Time Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000315/2019003-01 Open/Closed

[H.14] -

Conservative Bias 71152 The inspectors identified a finding of very low safety significance (i.e., Green) and an associated Non-Cited Violation (NCV) of Technical Specification (TS) 3.7.2, Steam Generator Stop Valves (SGVSs), when licensee personnel failed to have four Unit 1 SGSVs and associated actuator trains operable while in Mode 1 and subsequently failed to restore the affected SGSV actuator train and SGSV to an operable status or place Unit 1 in Mode 2 within the time limits specified by the associated TS Limiting Condition for Operation (LCO). In addition, a NCV of TS 3.0.4, LCO Applicability, was identified because the licensee entered a Mode of applicability without the SGSV actuator train and associated SGSV being operable as required. Specifically, the licensee failed to identify that Unit 1 #2 SGVS Train B Dump Valve MRV-222 was inoperable during a post-maintenance test (PMT) conducted on May 6, 2019; and subsequently entered Mode 1 contrary to TS 3.0.4 and operated for 21 days, contrary to TS 3.7.2.

Additional Tracking Items

Type Issue Number Title Report Section Status URI 05000315,05000316/20 18003-02 Site Specific Shielding and Barriers for HI-TRAC Transfer Cask Require NRC Approval Prior to Use 60855.1 Closed

PLANT STATUS

Unit 1 began the inspection period at rated thermal power. On September 29, 2019, the licensee reduced power to about 55 percent to repair a leak on a feedwater pump casing.

Unit 1 remained at or near 55 percent power for the remainder of the inspection period.

Unit 2 operated at or near rated thermal power until July 21, 2019, when the licensee shut down the unit in response to a degradation of Non-Essential Service Water (NESW) flow.

On July 25, 2019, the licensee restarted Unit 2. Unit 2 reached rated thermal power on July 26, 2019, and remained at or near rated thermal power until September 9, 2019, when Unit 2 began coast down operations prior to a scheduled refueling outage. On September 29, 2019, the licensee reduced power to about 50 percent to perform Main Steam Safety Valve testing. Following this testing, Unit 2 remained at or near 50 percent power for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

External Flooding Sample (IP Section 03.04) (1 Sample)

(1) The inspectors evaluated the licensee's readiness to cope with external flooding for the following area:
  • Screen House

71111.04Q - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Unit 1 Emergency Diesel Generator (EDG) AB and Associated Support Systems on July 8, 2019
(2) Unit 2 Residual Heat Removal (RHR) on July 23, 2019
(3) Unit 2 Turbine Driven Auxiliary Feedwater (TDAFW) Pump on August 8, 2019
(4) Unit 1 West Motor Driven Auxiliary Feedwater (MDAFW) Pump on August 14, 2019
(5) Unit 2 CD EDG on August 21, 2019

71111.04S - Equipment Alignment

Complete Walkdown Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated system configurations during a complete walkdown of the Unit 1 Qualified Offsite Power Lines on September 23, 2019

71111.05Q - Fire Protection

Quarterly Inspection (IP Section 03.01) (4 Samples)

The inspectors evaluated fire protection program implementation in the following selected areas:

(1) U2 CD EDG on July 7, 2019
(2) U2 AB EDG on July 7, 2019
(3) Auxiliary Building 573' Elevation on July 11, 2019
(4) U2 4 Kilovolt (kV) Switchgear Rooms AB and CD on July 11, 2019

71111.06 - Flood Protection Measures

Inspection Activities - Internal Flooding (IP Section 02.02a.) (1 Sample)

The inspectors evaluated internal flooding mitigation protection in the:

(1) Auxiliary Building, Elevations 573' and 587'

71111.07A - Heat Sink Performance

Annual Review (IP Section 02.01) (1 Sample)

The inspectors evaluated readiness and performance of:

(1) Unit 2 Non-Essential Service Water (NESW)

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the Control Room during a plant shutdown for a maintenance outage on July 21, 2019

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated licensed operator requalification training in the Unit 2 Simulator on September 12, 2019

71111.12 - Maintenance Effectiveness

Routine Maintenance Effectiveness Inspection (IP Section 02.01) (3 Samples)

The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:

(1) Unit 1 Auxiliary Feedwater (AFW)
(2) Unit 1 Main Feedwater
(3) Supplemental Emergency Diesel Generators (EDGs)

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (2 Samples)

The inspectors evaluated the risk assessments for the following planned and emergent work activities:

(1) Elevated Risk due to unplanned Unit 1 AB EDG inoperability on June 17, 2019
(2) Elevated Risk associated with the loss of Unit 2 NESW from July 21 through July 24, 2019

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 02.02) (5 Samples)

The inspectors evaluated the following operability determinations and functionality assessments:

(1) AR 2015-5237, Asymmetric Natural Circulation Cooldown with Low Decay Heat
(2) AR 2019-6882, Ice Condenser After Exceeding Notification Limit
(3) AR 2019-7053, PZR [Pressurizer] Insurge/Outsurge
(4) AR 2019-7919, Low Differential Pressure Across Fuel Handling Area Ventilation System Charcoal Bed
(5) Step Change in Differential Pressure (D/P) Across Auxiliary Fuel Handling Area Exhaust Filter

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (6 Samples)

The inspectors evaluated the following post maintenance tests:

(1) Mechanism-Operated Contact Switch Adjustment for Unit 1 AB EDG to 4kV Bus Supply Breaker; Work Order (WO) 55535235
(2) Unit 2 NESW Strainers following Cleaning, July 21 through 23, 2019
(3) Unit 2 East RHR Pump following Valve Work; WO 55359920
(4) Unit 1 CD EDG, on August 29, 2019, following planned maintenance
(5) Unit 1 TDAFW System on September 3, 2019, following planned maintenance
(6) Unit 1 East Component Cooling Water (CCW) Check Valve Flow Test following RCP
  1. 3 Lower Bearing CCW Throttle Valve Adjustment on September 13, 2019

71111.20 - Refueling and Other Outage Activities

Refueling/Other Outage Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated a Unit 2 maintenance outage from July 21 through July 25, 2019, which resulted from accumulated debris in the NESW strainers

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance test:

Surveillance Tests (other) (IP Section 03.01)

(1) Unit 2 New Fuel Receipt Inspections; WO 55518169 and WO 55518412

71114.06 - Drill Evaluation

Select Emergency Preparedness Drills and/or Training for Observation (IP Section 03.01) (1 Sample)

(1) Emergency Preparedness Drill on July 16, 2019

Drill/Training Evolution Observation (IP Section 03.02) (1 Sample)

The inspectors evaluated:

(1) Licensed Operator Requalification Training (LORT) with Drill Exercise Performance (DEP) on September 10,

RADIATION SAFETY

71124.08 - Radioactive Solid Waste Processing and Radioactive Material Handling, Storage,

and Transportation

Radioactive Material Storage (IP Section 02.01)

The inspectors evaluated radioactive material storage.

(1) The inspectors toured the following areas:
  • Radioactive Waste Drumming Room located in the Auxiliary Building 587'
  • Radioactive Waste Condensate Tanks South/North 587'
  • South Boric-Acid Evaporator Room 587
  • Radioactive Material Building and Contaminated Equipment Storage Area (CESA) Building where Dry Active Waste (DAW) Containers were Stored
  • Mausoleum Storage Area and CESA Contains Contaminated Equipment Stored in Sea-Lands

The inspectors performed a container check (e.g., swelling, leakage and deformation)on the following containers:

  • DAW Container No. 321; Air Compressors; dated February 19, 2013
  • DAW Container No. 314; Stinger Whip Welding Equipment; dated July 27, 2017
  • DAW Container No. 230; Spent Fuel Pool Tools and Spares; dated February 1, 2012
  • DAW Container No. 323; Camera Cables; dated February 1, 2013
  • DAW Container No. 102; Thimble Plugs Tools for Seal-Table; dated May 6, 2019
  • DAW Container No. 324; Power Packs and Electrical Transformers; dated March 14, 2016
  • DAW Container No. 226; Specimen Tools/Bolts for CRD Tools; dated April 28, 2019
  • DAW Container No. 237; CRDM [Control Rod Drive Mechanism] Equipment

Radioactive Waste System Walkdown (IP Section 02.02) (1 Sample)

The inspectors evaluated the following radioactive waste processing systems during plant walkdowns:

(1) Liquid or Solid Radioactive Waste Processing Systems
  • Radioactove Waste Drumming Room located in the Auxiliary Building 587 Resin Transfer/Sluicing System into a Liner/Cask
  • Energy Solution Liquid System; Radioactive Waste Water Demineralizer System
  • Spent Resin Storage Tank Resin Transfer System
  • DAW Trash Loading Located in the Auxiliary Building

Radioactive Waste Resin and/or Sludge Discharges Processes

  • Energy Solutions Liquid System; Radioactive Waste Water Demineralizer System
  • Spent Resin Storage Tank Resin Transfer System

Waste Characterization and Classification (IP Section 02.03) (1 Sample)

The inspectors evaluated the radioactive waste characterization and classification for the following waste streams:

(1) Shipping Cask Containing Spent Resin to Bear Creek, TN; Low Specific Activity (LSA-II)

Contaminated Equipment RAM [Radioactive Material] Shipment to Energy Solution Services as Surface Contaminated Objects (SCO-II)

Sample Shipment of 8 Samples to be Analyzed to GEL Laboratory as a Limited Quantity Material

Shipment Preparation (IP Section 02.04) (1 Sample)

The inspectors evaluated the following radioactive material shipment preparation processes:

(1) DCC18-053; UN3321, RAM LSA-II; Fissile Excepted; 7, RQ-1; Spent Resin Mixed Bed Ion Exchange Media to Bear Creek, TN; dated July 12, 2018 DCC18-074; UN3321, RAM LSA-II; Fissile Excepted; 7, RQ-1; Spent Resin Mixed Bed Ion Exchange Media to Bear Creek, TN; dated December 5, 2018 DCC19-053; UN2913, RAM SCO-II; Fissile Excepted; 7, RQ-1; Contaminated Equipment Contained in a Metal Box to Energy Solution Services, Memphis, TN; dated June 11, 2019

Shipping Records (IP Section 02.05) (1 Sample)

The inspectors evaluated the following non-excepted package shipment records:

(1) DCC18-059; UN3321, RAM LSA-II; Fissile Excepted; 7, RQ-1; Spent Resin Mixed Bed Ion Exchange Media to Bear Creek, TN in a Type-A Cask; dated June 11, 2019 DCC18-023; UN2910, RAM; Excepted Package; 7, Limited Quantity Material to GEL Labs; Containing Samples for 10CFR61 Analysis; dated March 18, DCC18-019; UN2910, RAM; Excepted Package; 7, Limited Quantity Material of Valves to Spartanburg, SC for Recertification; dated March 11,

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

BI01: Reactor Coolant System (RCS) Specific Activity Sample (IP Section 02.10)===

(1) PMP-7110-PIP-001; Reactor Oversight Program Performance Indicators (PIs) and Monthly Operating Report Data for Reactor Coolant Specific Activity; Unit 1; from January 1, 2018 through December 31, 2018
(2) PMP-7110-PIP-001; Reactor Oversight Program PIs and Monthly Operating Report Data for Reactor Coolant Specific Activity; Unit 2; from January 1, 2018 through December 31, 2018

71152 - Problem Identification and Resolution

Semiannual Trend Review (IP Section 02.02) (1 Sample)

(1) The inspectors reviewed licensee Nuclear Oversight reports, Nuclear Safety Review Board (NSRB) reports, and System Health summaries to identify potential adverse trends in documented issues that were not entered into the licensees corrective action program. The inspectors also assessed NRC findings to identify trends.

Annual Follow-up of Selected Issues (IP Section 02.03) (2 Samples 1 Partial)

The inspectors reviewed the licensees implementation of the corrective action program related to the following issues:

(1)

(Partial)

Missing Lateral Support Shim for Reactor Coolant Pump (RCP)-11

(2) Through-Wall Leak on Unit 1 RCP Seal Injection Lines
(3) Unit 1 Steam Generator Stop Valve Dump Valve Failed Surveillance

OTHER ACTIVITIES

- TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL

60855.1 - Operation of an Independent Spent Fuel Storage Installation at Operating Plants

Operation of an Independent Spent Fuel Storage Installation at Operating Plants (1 Partial)

(1)

(Partial)

The inspectors closed Unresolved Item 05000315/2018003-002; 05000316/2018003-02, Site Specific Shielding and Barriers for HI-TRAC Transfer Cask Require NRC Approval Prior to Use. The details of this review are documented in the inspection results below. No findings or violations were identified.

INSPECTION RESULTS

Unresolved Item (Closed)

Site Specific Shielding and Barriers for HI-TRAC Transfer Cask Require NRC Approval Prior to Use URI 05000315,05000316/2018003-02 60855.1

Description:

During the 2018 loading campaign, the licensee loaded spent fuel into Holtec Multi-Purpose Canister (MPC) 32 with Holtec International Transfer Cask (HI-TRAC) 125D. The site was using Holtec International Storage Module (HI-STORM) 100 CoC [Certificate of Compliance]

No. 1014, Amendment No. 9, Revision 1 (9R1). During the campaign, the licensee used additional shielding for As Low As Is Reasonably Achievable (ALARA) purposes. The additional shielding was in contact with the upper portions of the HI-TRAC and surrounding, but not in contact, with the HI-TRAC, which could hinder airflow or radiation heat transfer from the HI-TRAC. The licensee identified that the use of the shielding was not bounded by the conditions described in the cask Final Safety Analysis Report (FSAR) and subsequently requested Holtec to perform a site-specific thermal analysis to include the shielding. The site-specific thermal analysis contained inputs that were different than the design basis calculation inputs contained in the FSAR.

The licensee performed a 10 CFR 72.48 screening and evaluation, which concluded that the activity could be implemented without prior NRC approval. Subsequently, the 10 CFR 72.212 report was revised to allow the use of temporary shielding, and the licensee administratively imposed lower building temperatures limits and nuclear fuel assembly heat load limits from those specified in CoC No. 1014, Amendment No. 9R1, as determined in the site-specific thermal analysis. The licensee identified that the use of temporary shielding had the potential to result in CoC No. 1014, Amendment No. 9R1, Appendix B, Design Features, Section 3.9, and Approved Contents, Section 2.4, being non-conservative. Specifically, with the shielding in use, more restrictive requirements than those established in CoC No. 1014, Amendment No. 9R1 were necessary to ensure alignment with the FSAR safety analyses for peak cladding temperature (PCT) limits.

This issue was reviewed by the inspectors and technical specialists in the Division of Spent Fuel Management to determine compliance with Section 3.9 of CoC No. 1014, Amendment No. 9R1, Appendix B; potential non-conservatism of Section 3.9 of CoC No. 1014, Amendment No. 9R1, Appendix B; and compliance with 10 CFR 72.48(c)(1)(ii)(B).

Regarding whether the licensee was compliant with CoC No. 1014, Amendment No. 9R1; Appendix B, Section 3.9, Design Features, stated the following:

Short term operations involving the HI-TRAC transfer cask can be carried out if the reference ambient temperature (three-day average around the cask) is below the Threshold Temperature of 110 degrees F [Fahrenheit] ambient temperature, applicable during HI-TRAC transfer operations inside the 10 CFR Part 50 or 10 CFR Part 52 structural boundary and 90 degrees F outside of it. The determination of the Threshold Temperature compliance shall be made based on the best available thermal data for the site. If the reference ambient temperature exceeds the corresponding Threshold Temperature, then a site-specific analysis shall be performed using the actual heat load and reference ambient temperature equal to the three-day average to ensure that the steady state peak fuel cladding temperature will remain below the 400°C [degrees Celcius] limit.

While the above implied that a site-specific analysis was not necessary when the reference ambient temperature was below the corresponding threshold temperature, it did not preclude a site-specific analysis. Therefore, the licensee performed a site-specific analysis with the use of additional shielding and the administrative limits implemented by the licensee, which were bounded by the limits of Section 3.9 of Holtec CoC No. 1014, Amendment No. 9R1, Appendix B. Therefore, the licensee was compliant with Section 3.9 of Holtec CoC No. 1014, Amendment No. 9R1, Appendix B.

Regarding whether Section 3.9, Design Features, of CoC No. 1014, Amendment No. 9R1, Appendix B, was non-conservative, based on a review of Holtec Report No. HI-2177676, Thermal Evaluation of Shielding on HI-TRAC, which analyzed the transfer cask with temporary shielding in place, the inspectors determined that the use of the temporary shielding rendered the Design Features Section 3.9 and Approved Contents Section 2.4 of CoC No. 1014, Amendment No. 9R1, Appendix B as non-conservative. However, by performing a site-specific thermal analysis and imposing temperature and fuel loading restrictions, the licensee remained compliant with the requirements of CoC No. 1014, Amendment No. 9R1.

Regarding whether the licensee was compliant with 10 CFR 72.48(c)(1)(ii)(B), CNP 72.48 No.

7248-2018-0139-02, Thermal Evaluation of Shielding Package Around the HI-TRAC at D.C.

Cook, provided the 10 CFR 72.48 screening of the proposed activity. The licensee answered No to 10 CFR 72.48 Screening Question E., Does the proposed activity require a change to the ISFSI [Independent Spent Fuel Storage Installation] Technical Specifications or the CoC? The licensee provided the explanation, Calculation package (HI-2177676)provided technical results to demonstrate compliance with CoC No. 1014, Amendment 9, Revision 1.

Based on the determination that the licensee was compliant with Section 3.9 of CoC No.

1014, Amendment No. 9R1, Appendix B, the inspectors did not find any indication that the licensee was not in compliance with 10 CFR 72.48.

Since the licensee was compliant with CoC No. 1014, Amendment No. 9R1, Appendix B and 10 CFR 72.48, the inspectors consider this Unresolved Item closed.

Corrective Action References: AR 2018-4056, AR 2018-6342, and AR 2018-6642 Main Steam Stop Valve Dump Valve Inoperable for Longer than its Technical Specification Allowed Outage Time Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems

Green NCV 05000315/2019003-01 Open/Closed

[H.14] -

Conservative Bias 71152 The inspectors identified a finding of very low safety significance (i.e., Green) and an associated Non-Cited Violation (NCV) of Technical Specification (TS) 3.7.2, Steam Generator Stop Valves (SGVSs), when licensee personnel failed to have four Unit 1 SGSVs and associated actuator trains operable while in Mode 1 and subsequently failed to restore the affected SGSV actuator train and SGSV to an operable status or place Unit 1 in Mode 2 within the time limits specified by the associated TS Limiting Condition for Operation (LCO).

In addition, a NCV of TS 3.0.4, LCO Applicability, was identified because the licensee entered a Mode of applicability without the SGSV actuator train and associated SGSV being operable as required. Specifically, the licensee failed to identify that Unit 1 #2 SGVS Train B Dump Valve MRV-222 was inoperable during a post-maintenance test (PMT) conducted on May 6, 2019; and subsequently entered Mode 1 contrary to TS 3.0.4 and operated for 21 days, contrary to TS 3.7.2.

Description:

During Unit 1 Refueling Outage 29, and while in Mode 2, the licensee adjusted the packing on #2 SGSV Train B Dump Valve 1-MRV-222. This valve was part of the actuation system used to operate the #2 SGSV. On May 6, 2019, following the packing adjustment and prior to a Mode change, the licensee performed portions of the Unit 1 #2 SGSV Train B Dump Valve surveillance test as a post maintenance test. On the first attempt, the valve failed to stroke within the required maximum stroke time of 2 seconds. At that time, the licensee believed that the #2 SGSV Train B Dump Valve operated in a humid environment. To replicate this environment, the licensee wetted the #2 SGSV Train B Dump Valve packing and stem. The valve subsequently passed the surveillance test, the licensee declared the Unit 1 #2 SGSV Train B Dump Valve operable, and on May 9, 2019, transitioned Unit 1 from Mode 2 to Mode 1.

During the next scheduled Unit 1 #2 SGSV Train B Dump Valve surveillance test on May 29, 2019, the valve again failed to stroke within the 2 second stroke time limit. The licensee performed additional investigation and identified that the valve packing had hardened and required replacement. The licensee also identified that the environment that was assumed to exist during the previous troubleshooting effort had been incorrect and that, in fact, the #2 SGSV Train B Dump Valve operated in a non-humid (dry) environment, and therefore the packing was not wet during operation. The packing was replaced, and following a successful PMT the Unit 1 #2 SGSV Train B Dump Valve was returned to service.

During inspection activities to assess the licensees corrective actions, the inspectors identified that the licensee failed to identify that the Unit 1 #2 SGSV Train B Dump Valve and associated #2 SGSV was inoperable from the time Unit 1 entered Mode 1 on May 9, 2019, until the issue was corrected on May 30, 2019. Additionally, the licensee failed to assess the impact of this issue on operability. Following discussions with licensee staff, AR 2019-8511, Past ODE [Operability Determination Evaluation] Possibly Missed, was generated and an operability assessment was performed. This assessment was completed on September 24, 2019, and concluded that the Unit 1 #2 SGSV Train B Dump Valve and associated #2 SGSV was inoperable beginning with the transition to Mode 1 on May 9, 2019, until the valve packing was replaced on May 30, 2019.

Corrective Actions: The licensee performed a past operability assessment under AR 2019-8511. The deficient condition was corrected previously under AR 2019-5615 on May 30, 2019.

Corrective Action References: AR 2019-5615

Performance Assessment:

Performance Deficiency: The inspectors determined that the licensees failure to identify that the Unit 1 #2 SGSV Train B Dump Valve was inoperable during a PMT was a performance deficiency. Specifically, the PMT performed by the licensee created more favorable conditions for valve operation than what existed in the actual operating environment. As a result, the licensee failed to identify that the Unit 1 #2 SGSV Train B Dump Valve and associated #2 SGSV was inoperable.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Equipment Performance attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the finding resulted in one train of SGSV actuators being inoperable, causing a delay in the opening of the #2 SGSV and rendering the #2 SGSV also inoperable.

Significance: The inspectors assessed the significance of the finding using Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The inspectors answered Yes to Question A.2 in Exhibit 2 because the Unit 1 #2 SGSV Train B Dump Valve was inoperable for 21 days, which was greater than the TS 3.7.2 Allowed Outage Time of 7 days.

Therefore, a Detailed Risk Evaluation (DRE) was performed using Inspection Manual Chapter (IMC) 0609, Appendix A. The inspectors performed a bounding analysis by failing the Unit 1

  1. 2 SGSV Train B Dump Valve for 21 days and determined the delta core damage frequency (CDF) was 4.7E-9. As a result, the finding was determined to be of very low safety significance (i.e., Green).

Cross-Cutting Aspect: H.14 - Conservative Bias: Individuals use decision making-practices that emphasize prudent choices over those that are simply allowable. A proposed action is determined to be safe in order to proceed, rather than unsafe in order to stop. Specifically, when troubleshooting the Unit 1 #2 SGSV Train B Dump Valve after its failure on May 6, 2019, the licensee failed to validate the assumptions about the environment in which the valve operated. This caused the licensee to perform an inadequate PMT and ultimately fail to restore the valve to an operable status.

Enforcement:

Violation: Technical Specification 3.7.2, Steam Generator Stop Valves (SGSVs), required that in Mode 1 all four SGSVs and their associated actuator trains be operable. Technical Specification 3.7.2.A required that with one SGSV actuator train inoperable, that the SGSV actuator train be restored to an operable status within 7 days. Technical Specification 3.7.2.E required that if the required action and completion time of Technical Specification 3.7.2.A is not met, to declare each affected SGSV inoperable. Technical Specification 3.7.2.F, Steam Generator Stop Valves (SGSVs), required that with one SGSV inoperable in Mode 1 that the SGSV be restored to an operable status within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />. Technical Specification 3.7.2.G required that if the required action and associated completion time of Technical Specification 3.7.2.F is not met the Unit be placed in Mode 2 within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />.

Technical Specification 3.0.4 required that when a Limiting Condition for Operation is not met, that entry into a Mode applicable to a technical specification shall only be made when, a) the associated actions to be entered permit continued operation in the Mode in the applicability for an unlimited period of time, or b) after the performance of a risk assessment and the establishment of risk management actions, or c) when an allowance is stated in the individual value, parameter, or other specification.

Contrary to the above, on May 9, 2019, with Unit 1 in Mode 1 and with the #2 SGSV Train B Dump Valve, which was a part of the #2 SGSV actuator train, inoperable, the licensee failed to restore the inoperable #2 SGSV actuator train to an operable status within 7 days and failed to declare the associated #2 SGSV inoperable. Also, on May 9, 2019, with Unit 1 in Mode 1 and with the #2 SGSV inoperable, the licensee failed to restore the #2 SGSV to an operable status within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> as required by Technical Specification 3.7.2.F, and failed to place Unit 1 in Mode 2 within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> as required by Technical Specification 3.7.2.G. In addition, prior to entering Mode 1 from Mode 2 on May 9, 2019, with an inoperable SGSV and associated Limiting Condition for Operation 3.7.2.G that did not permit continued operation for an unlimited period of time and did not provide an allowance as stated in an individual value, parameter, or other specification, the licensee failed to perform a risk assessment and establish risk management actions as required by Technical Specification 3.0.4.

Enforcement Action: This violation is being treated as an non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On October 15, 2019, the inspectors presented the integrated inspection results to Mr. J. Gebbie, Senior VP and Chief Nuclear Officer, and other members of the licensee staff.
  • On August 8, 2019, the inspectors presented the Radioactive Material Processing/Transportation and RCS Specific Activity Performance Indicator inspection results to Mr. S. Lies, Site Vice President, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.04Q Corrective Action

Documents

2018-0075

U1 CD EDG Tripped Due to Air System Issues

01/02/2018

2018-0242

DG1CD Tripped on Overspeed During a Start

01/08/2018

2018-6841

Unit 1 CD EDG Not Synchronizing to T11D Bus

07/02/2018

2018-6917

Potential Commonality in Recent Repeat Events

07/05/2018

2018-9194

Unit 2 PAC Trip

09/27/2018

Drawings

1-OP-5151D-72

Flow Diagram Emergency Diesel Generator CD Unit 1

OP-1-5113A-9

Flow Diagram Essential Service Water

OP-1-5143-80

Flow Diagram Emergency Core Cooling (RHR) Unit No. 1

OP-1-5148C-30

Flow Diagram Diesel Generator Area & Electric Switchgear

Room Heating & Ventilation System Unit 1

OP-1-5151A-50

Flow Diagram Emergency Diesel Generator AB Unit 1

OP-1-5151C-58

Flow Diagram Emergency Diesel Generator CD Unit 1

OP-1-98013-42

Diesel Generator 1AB and Auxiliaries Elementary Diagram

OP-1-98014-40

Diesel Generator 1CD and Auxiliaries Elementary Diagram

OP-1-98016-41

Diesel Generator 1AB Miscellaneous Auxiliaries Elementary

Diagram

OP-1-98017-46

Diesel Generator 1CD Miscellaneous Auxiliaries Elementary

Diagram

OP-2-5143-75

Flow Diagram Emergency Core Cooling (RHR) Unit No. 2

OP-5151B-61

Flow Diagram Emergency Diesel Generator AB Unit #1

Procedures

1-OHP-4012-032-

008CD

Operating DG1CD Subsystems

1-OHP-4021-008-

2

Placing Emergency Core Cooling System in Standby

Readiness

1-OHP-4021-017-

001

Operation of the Residual Heat Removal System

1-OHP-4021-032-

008AB

Operation DG1AB Subsystems

1-OHP-4021-032-

008B

Operating DG1AB Subsystems

1-OHP-4030-156-

017E

East Motor Driven Auxiliary Feedwater System Test

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

2-OHP-4021-008-

Placing Emergency Core Cooling System in Standby

Readiness

2-OHP-4021-032-

008CD

Operating DG2CD Subsystems - DG2CD Starting Air

System Valves

2-OHP-4021-07-

001

Operation of the Residual Heat Removal System

2-OHP-4030-256-

017T

Turbine Driven Auxiliary Feedwater System Test

Work Orders

55501397

MTRI, 2-PPS-1, Calibrate/Replace as Necessary

71111.05Q Drawings

2-5972

Fire Hazards Analysis Plan Below Basement Units 1 and 2

2-5974

Fire Hazard Analysis Mezzanine Floor El. 609 Units 1 & 2

Fire Plans

Fire Pre-Plans Volume 1

Fire Zone 18

CD Diesel Generator Room, Unit 2 Elevation 587

Fire Zone 40A

kV AB Switchgear Room, Unit 1 Elevation 609-0

Fire Zone 47A

4kV AB Switchgear Room, Unit 2 Elevation 609-0

71111.06

Calculations

MD-12-Flood-

008-N

Flooding Due to Groundwater Level Increase, Cook Nuclear

Plant Flood Hazard Re-Evaluation

PRA-Flood-002

Internal Flooding Impact on Plant Power Distribution

PRA-Flood-004

Internal Flooding - Qualitative Screening Analysis

PRA-Flood-008

Flood Sources and Associated Flood Mechanisms

PRA-Flood-008

Appendix F

Rupture Flow Rates of Flood Sources

SD-061206-001

Flooding Evaluation Report for D.C. Cook Nuclear Power

Plant

Corrective Action

Documents

GT-2015-5625-23 Inspection Frequency for Interim Flood Measures

08/12/2015

Drawings

OP-1-5123A

Station Drainage - Auxiliary Building, Unit 1

OP-12-5123

Station Drainage Auxiliary Building

Procedures

1-OHP-4022

ESW System/Rupture

2-EHP-4075-

TCA-001

Operator Time Critical Actions

2-OHP-4027-

FSG-1501

Flooding Response Deployment

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.07A

Drawings

OP-1-5114-152

Flow Diagram Non-Essential Service Water Unit No. 1

OP-2-5114-93

Flow Diagram Non-Essential Service Water Unit No. 2

Procedures

1-OHP-4022

NESW System Loss/Rupture

2-OHP-4021-028-

018

Operation of the Containment Chilled Water System,

Figure 1, System Drawings

71111.11Q Miscellaneous

RQ-C-4431

Secondary Side Break & Pressurized Thermal Shock

Analysis

SOER 87-3

Pipe Failures in High Energy Systems Due to Erosion

Corrosion

04/02/1987

71111.12

Corrective Action

Documents

2019-5615-1

1-MRV-222 Failed Surveillance

05/29/2019

Miscellaneous

Two-year Unavailability Report for the Supplemental Diesel

Generator (SDG) System; SSC 12-SDG

09/25/2019

71111.15

Calculations

DC-D-01-CS-4

Piping and Pipe Support Analysis of CS and RC System for

EBASCO Walkdown Package Nos. CS-11 and RC-09

Corrective Action

Documents

2018-6093

Increasing Unit 1 CCW Out-Leakage

06/06/2018

2018-6615

Unidentified HELB Break Locations

06/26/2018

2018-7570-01

Operability Determination Evaluation (Unit 1 East CCW Heat

Exchanger Leak)

07/27/2018

2019-5237

Asymmetrical Natural Circulation Cooldown Issue with Low

Decay Heat

05/14/2019

2019-5666

Revise Procedure to Support TRM Update

05/30/2019

2019-7053

Pressurizer Insurge/Outsurge

AR 2019-6882

U2 Ice Bed Temps Above eSOMS Notification Limits

07/15/2019

AR 2019-7919

2-HV-AFX Charcoal D/P Outside of ESOMS Limits

08/19/2019

Drawings

1-CS-780-L1-2

Containment

OP-1-5129

CVCS-Reactor Letdown & Charging

OP-12-5148-63

Flow Diagram Auxiliary Building Ventilation Units 1 & 2

Engineering

Changes

0000055754

Install Mechanical Jumper to Connect the Essential Service

Water System to the Component Cooling Water System in

Either Unit to Provide a Source of Makeup Water to the

CCW System

Miscellaneous

FHA Exhaust Fan Charcoal Differential Pressure

08/23/2019

Temporary

Design, Install Mechanical Jumper to Connect the Essential

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Modification 12-

TM-15-49

Service Water System to the Component Cooling Water

System in Either Unit to Provide a Source of Makeup Water

to the CCW System

UFSAR Section 14.2.5

Rupture of a Steam Pipe

WCAP-14717

Evaluation of the Effects of Insurge/Outsurge Out-of-Limit

Transients on the Integrity of the Pressurizer Program

MUHP-5063 Summary Report

Procedures

2-OHP-4021-

016-003

Component Cooling Water System Operation

2-OHP-5030-

016-001

Supply ESW to CCW for Makeup Using Temporary

Modification

Work Orders

55504921-01

2-HV-AFX, Auxiliary Building Ventilation Fuel Handling

Area Exhaust Filter Unit, Replace Charcoal Bed

08/23/2017

55504921-02

2-HV-AFX, Auxiliary Building Ventilation Fuel Handling

Area Exhaust Filter Unit, Perform Test After Charcoal

Replacement

08/28/2017

71111.18

Procedures

OHI-4016

Conduct of Operations: Guidelines

71111.19

Corrective Action

Documents

2019-8353

Failed PMT 55533608-05, U1 CD Diesel has a Slight Leak

on the 1-R Jacket Water Outlet

08/30/2019

AR-2019-8528

Unit 1 East CCW Pump Surveillance was Aborted Due to #3

RCP CCW Flows

09/06/2019

Engineering

Evaluations

DIT-B-03787-01

Restoration of Component Cooling Water Flow to Unit 1

Reactor Coolant Pump #3 Motor Bearing Cooler

09/10/2019

Miscellaneous

Clearance Order

241552

2-IMO-312 Actuator

Procedures

1-OHP-4030-116-

20E

East Component Cooling Water Loop Surveillance Test

09/13/2019

1-OHP-4030-132-

27CD

CD Diesel Generator Operability Test (Train A), DG1CD

Fast Speed Start

2-OHP-4030-208-

053A

ECCS Valve Operability Test - Train A

Shipping Records 55518412-11

MTRS, (R2P) U2 Load New Fuel into SFP

Work Orders

55359920-10

OPS: 2-IMO-312, Stroke for PMT Operability

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

55518169-01

MTRS, (R2P) U2 Unload New 17x17 Fuel

55535360-14

MTM, 2-OME-35N Open NESW PP Strainer and Check for

Debris

97/21/2019

55535386-05

2-OME-35S MTM: 2-OME-35S; Open NESW Strainer and

Check for Debris

07/22/2019

WO Task:

55523374 01

1-FMO-231/Perform A-Found Diagnostic

71111.20

Miscellaneous

Forced Outage Critical Path

07/22/2019

Procedures

PMP-2291-OLR-

001

Technical Specification 3.0.4.b Risk Assessment Review

and Approval Form for Transitioning Modes with an

Intermediate Range Nuclear Instrument Inoperable

71114.06

Miscellaneous

2019 DC Cook DR1 Drill Manual

07/30/2019

2019 DC Cook

EMPE Manual

DC Cook EMPE Drill

07/16/2019

DR2 Drill

Scenario Manual

Dress Rehearsal 2 (Team 3)

August 13,

2019

EP-S-19DR2

2019 Dress Rehearsal #2

Procedures

RMT-2080-TSC-

001

Activation and Operation of the TSC

RMT-2080-TSC-

CHK-001

Site Emergency Director List

RMT-2080-TSC-

CHK-009

PET-Operations Checklist

71124.08

Calculations

PMP-2030-REC-

001

2016 10CFR61 Scaling Factor Report

11/08/2017

PMP-2030-REC-

001

2017 10CFR61 Scaling Factor Report

10/29/2018

Engineering

Evaluations

Technical 3002 8-

20A Cask

Cask Handling Procedure for USDOT Spec 7A, Type-A

Transportation Cask

05/14/2018

Self-Assessments GT-2018-1675

Self Assessment of the Radwaste Program at DC Cook that

Covers Radwaste Processing, Handling and Transportation

08/30/2018

Shipping Records DCC18-043

Compactible Trash to Energy Solution Bear Creek Facility

for Processing

05/10/2018

DCC18-044

A Box of Contaminated Equipment to Framatome, Inc.

05/16/2018

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

DCC18-059

Mixed Bed Ion Exchange Spent Resin for Processing to

Energy Solution Bear Creek, Oak Ridge,TN

07/24/2018

DCC18-074

Mixed Bed Resin PRC-1M; Class -B Shipment; UN3321;

LSA-II; RQ; Contained in a Shipping Cask Model 8-120B; to

Energy Solution for processing

11/30/2018

DCC19-033

UN2910 Excepted Package Limited Quantity of Steel Drum

for Part 61 Anlysis

04/15/2019

DCC19-038

Shipment of 2 Sea-Vans Containing Contaminated

Equipment to Westinghouse

04/25/2019

DCC19-041

Compacted Contaminated Trash to Unitech Services, TN

05/01/2019

DCC19-053

Sea-van on a Flatbed Trailer Containing a Shipment

Consigned as UN2913, SCOII Fissile Excepted

06/11/2019

71151

Calculations

PMP-7110-PIP-

001

Reactor Oversight Program Performance Indicators and

Monthly Operating Report Data for Reactor Coolant Specific

Activity; Unit 1 and 2

01/01/2018 -

2/31/2018

71152

Corrective Action

Documents

2019-2963

Investigate Reactor Coolant Pump Seal Injection Line Under

Suspicious Boric Acid Deposit

03/22/2019

2019-4341

Failure to Verify Procedure Directed Terminal Points

04/24/2019

2019-4734

Labeling in Unit 1 Lube Oil Tank Room Junction Box

05/03/2019

2019-4895

1-MRV-222 Failed Post Maintenance Test Timing

05/06/2019

2019-5615

1-MRV-222 Failed Surveillance

05/29/2019

2019-8511

Past Operability Determination Possible Missed

09/05/2019

Miscellaneous

Outage Control Center Shift Package

09/30/2019

Indiana Michigan Power 2019 Second Quarter Trend Report

AEP-19-005

Donald C. Cook Nuclear Plant Safety Review Board Meeting

03/04/2019

NOS-19-002

Nuclear Oversight Quarterly Report for October - December

2018

01/21/2019

NOS-19-006

Nuclear Oversight Quarterly Report for January - March

2019

04/23/2019

UCR 2215

UFSAR Change Request, Data Sheet 1 of PMP-2350-SAR-

001, UFSAR Update Process

Procedures

1-IHP-6040-171-

001

Verification of Turbine Support Systems Interlocks

20