ML19345H406: Difference between revisions
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O OPERATING OATA REPORT DOCKET NO. | O OPERATING OATA REPORT 50-293 DOCKET NO. | ||
.DATE ud/ u/ si COMPLETED BY G G. Whitney TELEPHONE 617-746-7900 OPERATING STATUS Pilgrim I Notes | |||
: 1. Unit Name: | : 1. Unit Name: | ||
April. 1981 l | April. 1981 l | ||
: 2. Reporting Period: | |||
1998. | 1998. | ||
: 3. LicensedThermalPower(MWt): | : 3. LicensedThermalPower(MWt): | ||
I | 678. | ||
I | |||
: 4. Nameplate Rating (Gross MWe): | |||
655. | |||
: 5. Design Electrical Rating (Net MWe): | : 5. Design Electrical Rating (Net MWe): | ||
90. | 90. | ||
: 6. Maximum Dependable Capacity (Gross MWe): | : 6. Maximum Dependable Capacity (Gross MWe): | ||
670. | |||
: 7. Maximum Dependable Capacity (Net MWe): | : 7. Maximum Dependable Capacity (Net MWe): | ||
: 3. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since List Report. Give Reasons: | : 3. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since List Report. Give Reasons: | ||
None | None | ||
: 9. Power Level To Which Restricted. If Any (Net MWe): | : 9. Power Level To Which Restricted. If Any (Net MWe): | ||
None | |||
: 10. Reasons For Restrictions,if Any: | : 10. Reasons For Restrictions,if Any: | ||
N/A This Month | N/A This Month Yr.-to.Date Cumulative i | ||
719.0 2879.0 73559.0 l | |||
: 12. Number Of Hours Reactor Was Critical | : 11. Hours In Reporting Period | ||
: 13. React- Reserve Shutdown Hours | : 12. Number Of Hours Reactor Was Critical 710.2 2603.6 52788.2 0.0 0.0 0.0 | ||
: 14. Hours Generator On-Line | : 13. React-Reserve Shutdown Hours | ||
: 15. Unit Reserve Shutdown Hours | : 14. Hours Generator On-Line 706.0 2574.6 51081.5 | ||
: 16. Gross Thermal Energy Generated (MWH) | : 15. Unit Reserve Shutdown Hours 0.0 0.0 0.0 | ||
17 Gross Electrical Energy Generated (Mk H) | : 16. Gross Thermal Energy Generated (MWH) 1316736.0 4590528.0 86879904.0 17 Gross Electrical Energy Generated (Mk H) 453930.O 1551960.0 28881324.0 IS. Net Electrical Eneqy Generated (MWH) 436753.0 1492720.0 27743327.0 98.2 89.4 69.4 | ||
1551960.0 | : 19. Unit Service Factor 98.2 69.4 o9.4 | ||
: 19. Unit Service Factor | : 20. Unit Availability Factor 90.7 77.4 jo.3 | ||
: 20. Unit Availability Factor | : 21. Unit Capacity Factor (Using MDC Net) 92./ | ||
: 21. Unit Capacity Factor (Using MDC Net) | /9.2 a/.o | ||
: 22. Unit Capacity Factor (Using DER Net, | : 22. Unit Capacity Factor (Using DER Net, 1.8 1.6 10.0 | ||
: 23. Unit Forced Outage Rate | |||
: 24. Shutdowns Scheduled Over Next 6 Months (Type. Date, and Duration of Each t: | : 24. Shutdowns Scheduled Over Next 6 Months (Type. Date, and Duration of Each t: | ||
Refuel Outage Commencing Septecher 1981 n | Refuel Outage Commencing Septecher 1981 n | ||
Operadng | |||
: 25. If Shut Down At End Of Report Period. Estimated Date of Startup: | : 25. If Shut Down At End Of Report Period. Estimated Date of Startup: | ||
: 26. Umts in Test Status (Prior to Commercial Operation): | : 26. Umts in Test Status (Prior to Commercial Operation): | ||
Forecast Achieved INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION 8105200 @ | |||
N/77) l | N/77) l | ||
AVERAGE DAILY UNITFOWER LEVEL DOCXET NO. | AVERAGE DAILY UNITFOWER LEVEL 50-293 DOCXET NO. | ||
63 3. | Pilgrim i WT DATE 5/12/81 COMPLETED BY G.G. Whitney 6 17-746-7900 TELEPHONE April, 1981 MONTH DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POV R LEVEL (Mwe-Net) | ||
(g w g.,3 668. | |||
3 655. | : 547, 1 | ||
4 462. | 63 3. | ||
294. | |||
6 487. | IS 656. | ||
307. | |||
3 | 3 39 655. | ||
9 | 599. | ||
637. | 4 2. | ||
10 665. | 462. | ||
662. | 670. | ||
g3 | 21 351. | ||
g3 658. | 668. | ||
g4 | 6 487. | ||
16 | 668. | ||
INSTRUCTIONS | 23 667. | ||
On th:s format.!ist the. average dany unit power level in MWe. Net for each day in the repcmng month. Campute to the nearest wncie megawatt. | 660. | ||
l (O f | 3 24 591. | ||
667. | |||
9 25 637. | |||
636. | |||
10 | |||
:s 665. | |||
661. | |||
662. | |||
656. | |||
g3 3 | |||
662. | |||
649. | |||
g3 658. | |||
644. | |||
g4 30 656. | |||
o 15 3g 655. | |||
16 INSTRUCTIONS On th:s format.!ist the. average dany unit power level in MWe. Net for each day in the repcmng month. Campute to the nearest wncie megawatt. | |||
l (O | |||
l f | |||
l 1 | l 1 | ||
IM)CKEI NO. | 50-293 IM)CKEI NO. | ||
IINil SilllllM)WNS ANI) POWER REDilCIIONS UNII NAME Pilgrim I DAIE _5U2L81 CoMrs.E IED liv _n.__G.__Witit.ncy. | |||
RI I'OR I' MON ill APRIL, 1981 | RI I'OR I' MON ill APRIL, 1981 IEl.EriloNE _(il7-746-7900 l | ||
"L jE 3 | |||
. E' IIrensee Eg | |||
~L Cause & Cenicctive 8 | |||
Action to No. | |||
D.it e g-3g s | |||
13.0 | ,yu Event gg gU I-y.3 cE 5@C Iteport if | ||
'd U Paesent Iletureceire o | |||
l U | |||
b 6 | |||
81/04/05 S | |||
0.0 B | |||
5 N.A. | |||
IIC llTEXCll Main Condenser Backwash 4 | |||
) | |||
7 81/04/06 F | |||
13.0 A | |||
3 N.A. | |||
Z 7. | |||
ZZZZZZ Unit trip due to high level in | |||
'C' innisture separator. | |||
l J | l J | ||
B | B 81/04/18 S | ||
0.0 B | |||
5 N.A. | |||
IIC IITEXCil Repnirs inade to 'B' 3rd point henter f | |||
expansion joint I | |||
i i | i i | ||
i 4 | i 4 | ||
| Line 95: | Line 135: | ||
i 4 | i 4 | ||
i 1 | i 1 | ||
i | j i | ||
4 F: l'orteil | 2 3 | ||
S: Sc hriinics | 4 F: l'orteil Reason: | ||
D Regulatory Restriction | Methoil: | ||
G Operational fision (1.xplain) | Enhihlt (; - Instnitilims 4 | ||
1 S: Sc hriinics A Eqtilyment Falluse(Explain) 1 -Manual for Picparation of Data B Maintenance of Test 2-Manual Scram. | |||
Entry Sheets for I.icensce C Ilefueling 3 Automatic Scram. | |||
Event Repost (l.1:ltil'ile tNilRl(;. | |||
D Regulatory Restriction 4.Othes (Explain) 01611 E Operator Tralning A IIrense I:xamination i | |||
F.Administ atIve 5 | |||
l G Operational fision (1.xplain) 13hibit 1 - Same Somre I'8/if ) | |||
II Ollies (Explain) | |||
L DE TA I | |||
D E | CO S | ||
D S | |||
A E | |||
C | |||
!!OE 1t I | |||
R TR CU AC m | |||
E e | |||
ER t | |||
r V | |||
s e | |||
T 1 | |||
y k | |||
TN S | |||
a CE t | |||
e EV n | |||
s r | |||
RE i | |||
e B | |||
RR T | |||
OP s | |||
d C | |||
e g | |||
e O | |||
l n | |||
r T | |||
c i | |||
e s | |||
m d | |||
u i | |||
r M | |||
T O | |||
E C | |||
N AN E | |||
E T | |||
C s | |||
N N | |||
e A | |||
b d | |||
I A | |||
l d | |||
u e | |||
l t | |||
E e | |||
T n | |||
t T | |||
k r | |||
e D | |||
N c | |||
n i | |||
t E | |||
I a | |||
a a | |||
h e | |||
T A | T A | ||
I | p e | ||
p g | |||
A. | |||
C | I e | ||
l e | |||
i I | |||
R C | |||
C | R T | ||
l. | |||
IR YTE F | |||
d | E gg d | ||
S nn e | |||
n l | |||
l ii gs e | |||
a | A kd ge k | ||
~ | |||
C R | |||
~ | |||
cn ub o | |||
0 | |||
~ | |||
ai l u r | |||
1 PB PT B | |||
e A | |||
t | |||
~ | |||
i l | |||
k a | |||
c n | |||
o i | |||
!O l | |||
m I | |||
p r | |||
r T | |||
o e | |||
e C | |||
n w | |||
t T | |||
N I | |||
o n | |||
U l | |||
i d | |||
F e | |||
F e | |||
L v | |||
r t | |||
A l | |||
w o | |||
a a | |||
o o | |||
e 1 | |||
1 V | |||
L D | |||
l l | |||
ne G o. | |||
T b p N | |||
7 l r m E | |||
1 euo N | |||
sTC O | |||
1 B | |||
6 e | |||
0 1 | |||
i rt PI 3 | |||
9 D os to 1 | |||
0 1 | 0 1 | ||
t i A | |||
C 2 | |||
0 | |||
" as O | |||
3 B rs M | |||
E 1 | |||
" cA H | |||
E T | |||
3 0 | |||
6 9 | |||
2 S | |||
1 3 | |||
2 Y | |||
S 4 | |||
,1 ij: | |||
14 J | |||
E | l | ||
PILGRIM NUCLEAR POWER STATION 4 | |||
==SUMMARY== | ==SUMMARY== | ||
OF OPERATIONS FOR APRIL, 1981 On April 1,1981, PNPS was operating at 100% reactor power. With minor power reductions for condenser delta tegerature, the unit operated at 100% until April 4, when power was reduced to 50% for a condenser backwash. | OF OPERATIONS FOR APRIL, 1981 On April 1,1981, PNPS was operating at 100% reactor power. With minor power reductions for condenser delta tegerature, the unit operated at 100% until April 4, when power was reduced to 50% for a condenser backwash. | ||
On April 6, while operating at 100%, a unit trip occurred while investigating problems with moisture separator level controls. High level in "C" moisture separator resulter'. in a turbine trip which scrammad the reactor. The unit was taken criticci and returned to 100% at 1800 hours on April 7. | On April 6, while operating at 100%, a unit trip occurred while investigating problems with moisture separator level controls. High level in "C" moisture separator resulter'. in a turbine trip which scrammad the reactor. The unit was taken criticci and returned to 100% at 1800 hours on April 7. | ||
On April 9, the power was reduced to 75% to allow the 3rd point heater on 'B' feedwater train to be removed from service to repair a crack in the expansion joint. The unit was returned to 100% peyer on April 10 and continued at this level, with minor reductions for eta. denser delta temperature, until April 18. | On April 9, the power was reduced to 75% to allow the 3rd point heater on 'B' feedwater train to be removed from service to repair a crack in the expansion joint. | ||
The unit was returned to 100% peyer on April 10 and continued at this level, with minor reductions for eta. denser delta temperature, until April 18. | |||
Da April 18 the unit was reduced to 50% power to mechanically clean the con-de:nser tubes and backwash. | Da April 18 the unit was reduced to 50% power to mechanically clean the con-de:nser tubes and backwash. | ||
The unit was returned to 100% power on April 20 and continued at this power until the end of the month with minor reductions for condenser delta temperature. | The unit was returned to 100% power on April 20 and continued at this power until the end of the month with minor reductions for condenser delta temperature. | ||
SAFETY / RELIEF VALVE CHALLENGES MR | SAFETY / RELIEF VALVE CHALLENGES MR APRIL, 1981 Report Requirement: TMI T.A.P. II.K.3.3 No challenges for the month. | ||
m | |||
m | |||
..c RN ING IN70pl!ATION | |||
RN ING IN70pl!ATION | ~he following refueling infor=ation is included in the P.cn hly Repor: as requested in a letter :o Mr. C. C. Andegnini da:ed Januan IS,1973: | ||
For your con tenience, :he infor:a:1on supplied has been enu=ars:e.d so tha: | For your con tenience, :he infor:a:1on supplied has been enu=ars:e.d so tha: | ||
each nu=ber cc responds to equivalen: notation u:111:ed in :he request. | each nu=ber cc responds to equivalen: notation u:111:ed in :he request. | ||
1. | |||
*he na=a of this facill:7 is ?ilgri:: Nuclea: ?ower Sca:1ce, Occke: | |||
Nu=ber 50-29 3. | Nu=ber 50-29 3. | ||
2. | |||
Scheduled date for nex: Refueling Shu:down: | |||
Sep:e=ber. 1981 3. | |||
Scheduled date for restar: following refueling: | |||
4. | 4. | ||
3. | |||
Due :o their s1=ilarin, recuests i, 5, & 6 are responded to collec:17ely: | |||
6. | |||
The fuel, which had been loaded during the 1980 scheduled refueling is of the new ?SxfR design, consis:ing of appro:c1=a:ely 64 ou: age, | |||
(b) ~here are 764 fuel asse=clies in :he spent fuel pool | ?SLR3232 assecblies and 120 ?SD?3265 asse=blies. | ||
S. | 7. | ||
(a) | |||
~here are 580 fuel assemblies in the core. | |||
(b) ~here are 764 fuel asse=clies in :he spent fuel pool. | |||
S. | |||
(a) he sta:1on is presently licensed :o s: ore 2220 spen: fuel assecolies. | |||
~he ac:ual spen fuel s:orage capacin is 1770 fuel assa:blies a: | |||
presen:. | presen:. | ||
~ e planned spen: fuel s:orage capacin is 2320 fual assemblies. | |||
(b) n 9. | |||
apacip :o acco odate an addi:ional 1006 fuel assenblies. | %'i:h presen: spen: fuel in s:orage, che spen: fuel pool now has :he apacip :o acco odate an addi:ional 1006 fuel assenblies. | ||
i 1 | l i | ||
l | 1 l | ||
( | ( | ||
l | l | ||
| Line 189: | Line 335: | ||
1 i | 1 i | ||
P00RDMl!N l | P00RDMl!N l | ||
__.}} | |||
Latest revision as of 07:05, 24 December 2024
| ML19345H406 | |
| Person / Time | |
|---|---|
| Site: | Pilgrim |
| Issue date: | 05/12/1981 |
| From: | Whitney G BOSTON EDISON CO. |
| To: | |
| Shared Package | |
| ML19345H405 | List: |
| References | |
| NUDOCS 8105200247 | |
| Download: ML19345H406 (6) | |
Text
.
O OPERATING OATA REPORT 50-293 DOCKET NO.
.DATE ud/ u/ si COMPLETED BY G G. Whitney TELEPHONE 617-746-7900 OPERATING STATUS Pilgrim I Notes
- 1. Unit Name:
April. 1981 l
- 2. Reporting Period:
1998.
- 3. LicensedThermalPower(MWt):
678.
I
- 4. Nameplate Rating (Gross MWe):
655.
- 5. Design Electrical Rating (Net MWe):
90.
- 6. Maximum Dependable Capacity (Gross MWe):
670.
- 7. Maximum Dependable Capacity (Net MWe):
- 3. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since List Report. Give Reasons:
None
- 9. Power Level To Which Restricted. If Any (Net MWe):
None
- 10. Reasons For Restrictions,if Any:
N/A This Month Yr.-to.Date Cumulative i
719.0 2879.0 73559.0 l
- 11. Hours In Reporting Period
- 12. Number Of Hours Reactor Was Critical 710.2 2603.6 52788.2 0.0 0.0 0.0
- 13. React-Reserve Shutdown Hours
- 14. Hours Generator On-Line 706.0 2574.6 51081.5
- 15. Unit Reserve Shutdown Hours 0.0 0.0 0.0
- 16. Gross Thermal Energy Generated (MWH) 1316736.0 4590528.0 86879904.0 17 Gross Electrical Energy Generated (Mk H) 453930.O 1551960.0 28881324.0 IS. Net Electrical Eneqy Generated (MWH) 436753.0 1492720.0 27743327.0 98.2 89.4 69.4
- 19. Unit Service Factor 98.2 69.4 o9.4
- 20. Unit Availability Factor 90.7 77.4 jo.3
- 21. Unit Capacity Factor (Using MDC Net) 92./
/9.2 a/.o
- 22. Unit Capacity Factor (Using DER Net, 1.8 1.6 10.0
- 23. Unit Forced Outage Rate
- 24. Shutdowns Scheduled Over Next 6 Months (Type. Date, and Duration of Each t:
Refuel Outage Commencing Septecher 1981 n
Operadng
- 25. If Shut Down At End Of Report Period. Estimated Date of Startup:
- 26. Umts in Test Status (Prior to Commercial Operation):
Forecast Achieved INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION 8105200 @
N/77) l
AVERAGE DAILY UNITFOWER LEVEL 50-293 DOCXET NO.
Pilgrim i WT DATE 5/12/81 COMPLETED BY G.G. Whitney 6 17-746-7900 TELEPHONE April, 1981 MONTH DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POV R LEVEL (Mwe-Net)
(g w g.,3 668.
- 547, 1
63 3.
294.
IS 656.
307.
3 39 655.
599.
4 2.
462.
670.
21 351.
668.
6 487.
668.
23 667.
660.
3 24 591.
667.
9 25 637.
636.
10
- s 665.
661.
662.
656.
g3 3
662.
649.
g3 658.
644.
g4 30 656.
o 15 3g 655.
16 INSTRUCTIONS On th:s format.!ist the. average dany unit power level in MWe. Net for each day in the repcmng month. Campute to the nearest wncie megawatt.
l (O
l f
l 1
50-293 IM)CKEI NO.
IINil SilllllM)WNS ANI) POWER REDilCIIONS UNII NAME Pilgrim I DAIE _5U2L81 CoMrs.E IED liv _n.__G.__Witit.ncy.
RI I'OR I' MON ill APRIL, 1981 IEl.EriloNE _(il7-746-7900 l
"L jE 3
. E' IIrensee Eg
~L Cause & Cenicctive 8
Action to No.
D.it e g-3g s
,yu Event gg gU I-y.3 cE 5@C Iteport if
'd U Paesent Iletureceire o
l U
b 6
81/04/05 S
0.0 B
5 N.A.
IIC llTEXCll Main Condenser Backwash 4
)
7 81/04/06 F
13.0 A
3 N.A.
Z 7.
ZZZZZZ Unit trip due to high level in
'C' innisture separator.
l J
B 81/04/18 S
0.0 B
5 N.A.
IIC IITEXCil Repnirs inade to 'B' 3rd point henter f
expansion joint I
i i
i 4
l 1
i 4
i 1
j i
2 3
4 F: l'orteil Reason:
Methoil:
Enhihlt (; - Instnitilims 4
1 S: Sc hriinics A Eqtilyment Falluse(Explain) 1 -Manual for Picparation of Data B Maintenance of Test 2-Manual Scram.
Entry Sheets for I.icensce C Ilefueling 3 Automatic Scram.
Event Repost (l.1:ltil'ile tNilRl(;.
D Regulatory Restriction 4.Othes (Explain) 01611 E Operator Tralning A IIrense I:xamination i
F.Administ atIve 5
l G Operational fision (1.xplain) 13hibit 1 - Same Somre I'8/if )
II Ollies (Explain)
L DE TA I
CO S
D S
A E
C
!!OE 1t I
E e
ER t
r V
s e
T 1
y k
TN S
a CE t
e EV n
s r
RE i
e B
RR T
OP s
d C
e g
e O
l n
r T
c i
e s
m d
u i
r M
T O
E C
N AN E
E T
C s
N N
e A
b d
I A
l d
u e
l t
E e
T n
t T
k r
e D
N c
n i
t E
I a
a a
h e
T A
p e
p g
A.
I e
l e
i I
R C
R T
l.
IR YTE F
E gg d
S nn e
n l
l ii gs e
A kd ge k
~
C R
~
cn ub o
0
~
ai l u r
1 PB PT B
e A
t
~
i l
k a
c n
o i
!O l
m I
p r
r T
o e
e C
n w
t T
N I
o n
U l
i d
F e
F e
L v
r t
A l
w o
a a
o o
e 1
1 V
L D
l l
ne G o.
T b p N
7 l r m E
1 euo N
sTC O
1 B
6 e
0 1
i rt PI 3
9 D os to 1
0 1
t i A
C 2
0
" as O
3 B rs M
E 1
" cA H
E T
3 0
6 9
2 S
1 3
2 Y
S 4
,1 ij:
14 J
l
PILGRIM NUCLEAR POWER STATION 4
SUMMARY
OF OPERATIONS FOR APRIL, 1981 On April 1,1981, PNPS was operating at 100% reactor power. With minor power reductions for condenser delta tegerature, the unit operated at 100% until April 4, when power was reduced to 50% for a condenser backwash.
On April 6, while operating at 100%, a unit trip occurred while investigating problems with moisture separator level controls. High level in "C" moisture separator resulter'. in a turbine trip which scrammad the reactor. The unit was taken criticci and returned to 100% at 1800 hours0.0208 days <br />0.5 hours <br />0.00298 weeks <br />6.849e-4 months <br /> on April 7.
On April 9, the power was reduced to 75% to allow the 3rd point heater on 'B' feedwater train to be removed from service to repair a crack in the expansion joint.
The unit was returned to 100% peyer on April 10 and continued at this level, with minor reductions for eta. denser delta temperature, until April 18.
Da April 18 the unit was reduced to 50% power to mechanically clean the con-de:nser tubes and backwash.
The unit was returned to 100% power on April 20 and continued at this power until the end of the month with minor reductions for condenser delta temperature.
SAFETY / RELIEF VALVE CHALLENGES MR APRIL, 1981 Report Requirement: TMI T.A.P. II.K.3.3 No challenges for the month.
m
..c RN ING IN70pl!ATION
~he following refueling infor=ation is included in the P.cn hly Repor: as requested in a letter :o Mr. C. C. Andegnini da:ed Januan IS,1973:
For your con tenience, :he infor:a:1on supplied has been enu=ars:e.d so tha:
each nu=ber cc responds to equivalen: notation u:111:ed in :he request.
1.
- he na=a of this facill:7 is ?ilgri:: Nuclea: ?ower Sca:1ce, Occke:
Nu=ber 50-29 3.
2.
Scheduled date for nex: Refueling Shu:down:
Sep:e=ber. 1981 3.
Scheduled date for restar: following refueling:
4.
3.
Due :o their s1=ilarin, recuests i, 5, & 6 are responded to collec:17ely:
6.
The fuel, which had been loaded during the 1980 scheduled refueling is of the new ?SxfR design, consis:ing of appro:c1=a:ely 64 ou: age,
?SLR3232 assecblies and 120 ?SD?3265 asse=blies.
7.
(a)
~here are 580 fuel assemblies in the core.
(b) ~here are 764 fuel asse=clies in :he spent fuel pool.
S.
(a) he sta:1on is presently licensed :o s: ore 2220 spen: fuel assecolies.
~he ac:ual spen fuel s:orage capacin is 1770 fuel assa:blies a:
presen:.
~ e planned spen: fuel s:orage capacin is 2320 fual assemblies.
(b) n 9.
%'i:h presen: spen: fuel in s:orage, che spen: fuel pool now has :he apacip :o acco odate an addi:ional 1006 fuel assenblies.
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