IR 05000461/2005009: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
(Created page by program invented by StriderTol)
Line 18: Line 18:


=Text=
=Text=
{{#Wiki_filter:January 30, 2006 Mr. Christopher President and Chief Nuclear Officer
{{#Wiki_filter:ary 30, 2006


Exelon Nuclear
==SUBJECT:==
 
CLINTON POWER STATION NRC INTEGRATED INSPECTION REPORT 05000461/2005009
Exelon Generation Company, LLC
 
4300 Winfield Road
 
Warrenville, IL 60555SUBJECT:CLINTON POWER STATION NRC INTEGRATED INSPECTION REPORT 05000461/2005009


==Dear Mr. Crane:==
==Dear Mr. Crane:==
On December 31, 2005, the US Nuclear Regulatory Commission (NRC) completed an integrated inspection at your Clinton Power Station. The enclosed report documents the
On December 31, 2005, the US Nuclear Regulatory Commission (NRC) completed an integrated inspection at your Clinton Power Station. The enclosed report documents the inspection findings which were discussed on January 12, 2006, with Mr. R. Bement and other members of your staff.


inspection findings which were discussed on January 12, 2006, with Mr. R. Bement and other
This inspection examined activities conducted under your license as they relate to safety and to compliance with the Commissions rules and regulations and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
 
members of your staff.
 
This inspection examined activities conducted under your license as they relate to safety and to compliance with the Commission's rules and regulations and with the conditions of your
 
license. The inspectors reviewed selected procedures and records, observed activities, and
 
interviewed personnel.


Based on the results of this inspection, the inspectors identified two findings of very low safety significance (Green). Both of these findings involved violations of NRC requirements.
Based on the results of this inspection, the inspectors identified two findings of very low safety significance (Green). Both of these findings involved violations of NRC requirements.


However, because these violations were of very low safety significance and because the issues have been entered into the licensee's corrective action program, the NRC is treating
However, because these violations were of very low safety significance and because the issues have been entered into the licensees corrective action program, the NRC is treating these issues as non-cited violations, in accordance with Section VI.A.1 of the NRCs Enforcement Policy.
 
these issues as non-cited violations, in accordance with Section VI.A.1 of the NRC's
 
Enforcement Policy.
 
If you contest the subject or severity of a non-cited violation, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear
 
Regulatory Commission, ATTN.: Document Control Desk, Washington, DC 20555-0001; with
 
copies to the Regional Administrator, US Nuclear Regulatory Commission - Region III, 2443 Warrenville Road, Lisle, IL 60532-4352; the Director, Office of Enforcement, US Nuclear
 
Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector Office at
 
the Clinton Power Station Facility.
 
C. Crane-2-In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document
 
Room or from the Publicly Available Reco rds (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at


http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
If you contest the subject or severity of a non-cited violation, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, US Nuclear Regulatory Commission - Region III, 2443 Warrenville Road, Lisle, IL 60532-4352; the Director, Office of Enforcement, US Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector Office at the Clinton Power Station Facility. In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).


Sincerely,
Sincerely,
/RA/Mark A. Ring, Chief Branch 1 Division of Reactor Projects Docket No. 50-461 License No. NPF-62Enclosure:Inspection Report No. 05000461/2005009 w/Attachment: Supplemental Informationcc w/encl:Site Vice President - Clinton Power Station Plant Manager - Clinton Power Station
/RA/
 
Mark A. Ring, Chief Branch 1 Division of Reactor Projects Docket No. 50-461 License No. NPF-62 Enclosure: Inspection Report No. 05000461/2005009 w/Attachment: Supplemental Information cc w/encl: Site Vice President - Clinton Power Station Plant Manager - Clinton Power Station Regulatory Assurance Manager - Clinton Power Station Chief Operating Officer Senior Vice President - Nuclear Services Vice President - Operations Support Vice President - Licensing and Regulatory Affairs Manager Licensing - Clinton Power Station Senior Counsel, Nuclear, Mid-West Regional Operating Group Document Control Desk - Licensing
Regulatory Assurance Manager - Clinton Power Station
 
Chief Operating Officer
 
Senior Vice President - Nuclear Services
 
Vice President - Operations Support
 
Vice President - Licensing and Regulatory Affairs
 
Manager Licensing - Clinton Power Station
 
Senior Counsel, Nuclear, Mid-West Regional Operating Group
 
Document Control Desk - Licensing


=SUMMARY OF FINDINGS=
=SUMMARY OF FINDINGS=
IR 05000461/2005009; AmerGen Energy Company
IR 05000461/2005009; AmerGen Energy Company LLC; 10/01/2005 - 12/31/2005; Clinton


LLC; 10/01/2005 - 12/31/2005; Clinton Power Station; Post Maintenance Testing and Surveillance Testing.
Power Station; Post Maintenance Testing and Surveillance Testing.


This report covers a 3-month period of baseline resident inspection and announced baseline inspections on radiation protection, emergency preparedness and licensed operator requalification. The inspection was conducted by Region III inspectors and the resident inspectors. Two Green findings involving two non-cited violations (NCVs) were identified. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using
This report covers a 3-month period of baseline resident inspection and announced baseline inspections on radiation protection, emergency preparedness and licensed operator requalification. The inspection was conducted by Region III inspectors and the resident inspectors. Two Green findings involving two non-cited violations (NCVs) were identified. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.


Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SDP). Findings for which the SDP does not apply may be "Green" or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 3, dated July 2000.A.Inspector-Identified and Self Revealing Findings
A.     Inspector-Identified and Self Revealing Findings


===Cornerstone: Mitigating Systems===
===Cornerstone: Mitigating Systems===
: '''Green.'''
: '''Green.'''
A self-revealing finding involving a non-cited violation (NCV) of Technical Specification 5.4.1 "Procedures," was identified. On September 30, 2005, the
A self-revealing finding involving a non-cited violation (NCV) of Technical Specification 5.4.1 Procedures, was identified. On September 30, 2005, the Division III emergency diesel generator failed to properly run following maintenance activities, due to the inadequate maintenance instructions. The inadequate maintenance instructions resulted in air being trapped in the governor oil system during the replacement of the governor's servo booster motor. The licensee determined that this issue was the result of a maintenance planners failure to follow administrative guidelines for technical review during the development of the maintenance instructions.
 
Division III emergency diesel generator failed to properly run following maintenance activities, due to the inadequate maintenance instructions. The inadequate maintenance instructions resulted in air being trapped in the governor oil system during the replacement of the governor's servo booster motor. The licensee determined that this issue was the result of a maintenance planner's failure to follow administrative guidelines for technical review during the development of the maintenance instructions.


This issue resulted in extended outage and unavailability time for the emergency diesel generator.
This issue resulted in extended outage and unavailability time for the emergency diesel generator.


The inspectors determined that despite the fact that the issue involved work in progress, this issue was more than minor because the finding affected the Mitigating
The inspectors determined that despite the fact that the issue involved work in progress, this issue was more than minor because the finding affected the Mitigating Systems Cornerstone objective of ensuring the availability of mitigating systems to prevent undesirable consequences. The issue resulted in the emergency diesel generator being unavailable for longer than expected by the plant staff. Following the initial maintenance run of the diesel generator, operators declared that the diesel generator was available for use if needed to respond to an event. Corrective actions by the licensee included developing lesson-learned information to share with other maintenance planners. Additionally, the licensee planned to add technical guidance related to venting air from the diesel governor to the diesel maintenance training material. The finding also affected the cross cutting area of human performance since the licensees maintenance personnel failed to request technical guidance from the site engineering staff as directed by the licensees administrative procedures.


Systems Cornerstone objective of ensuring the availability of mitigating systems to prevent undesirable consequences. The issue resulted in the emergency diesel generator being unavailable for longer than expected by the plant staff. Following the initial maintenance run of the diesel generator, operators declared that the diesel generator was available for use if needed to respond to an event. Corrective actions by the licensee included developing lesson-learned information to share with other maintenance planners. Additionally, the licensee planned to add technical guidance related to venting air from the diesel governor to the diesel maintenance training material. The finding also affected the cross cutting area of human performance since the licensee's maintenance personnel failed to request technical guidance from the site engineering staff as directed by the licensee's administrative procedures.
        (Section 1R19)
 
: '''Green.'''
(Section 1R19)  
The inspectors identified a finding involving a non-cited violation for inadequate corrective action. The licensees failure to properly identify and correct a degraded electrical circuit in 2004, involving a high resistance connection on a fuse holder, resulted in the Division II emergency diesel generator subsystem being vulnerable to electrical circuit failure if called upon to complete its support function. The high resistance connection was caused by degraded grease-like material and dirt. This issue also resulted in the Division II diesel generator failure during a subsequent surveillance test.
 
3*Green. The inspectors identified a finding involving a non-cited violation for inadequate corrective action. The licensee's failure to properly identify and correct a degraded electrical circuit in 2004, involving a high resistance connection on a fuse holder, resulted in the Division II emergency diesel generator subsystem being vulnerable to electrical circuit failure if called upon to complete its support function. The high resistance connection was caused by degraded grease-like material and dirt. This issue also resulted in the Division II diesel generator failure during a subsequent surveillance test. The inspectors determined that the finding was greater than minor because the finding affected the Mitigating Systems Cornerstone objective of ensuring the availability, reliability, and capability of mitigating systems to prevent undesirable consequences.


The Division II emergency diesel generator 125 VDC system is a backup to the AC oil system in case of a loss of offsite power.
The inspectors determined that the finding was greater than minor because the finding affected the Mitigating Systems Cornerstone objective of ensuring the availability, reliability, and capability of mitigating systems to prevent undesirable consequences.


Offsite power was not lost, therefore, there was not an actual loss of safety function for the diesel. Corrective actions by the licensee included replacing the fuse and fuse holder and expediting actions to address the extent of condition relative to the as-found condition of the fuse and fuse holder. The finding also affected the cross cutting area of problem identification and resolution since the licensee failed to adequately address the degraded circuit condition in a timely manner. (Section 1R22)  
The Division II emergency diesel generator 125 VDC system is a backup to the AC oil system in case of a loss of offsite power. Offsite power was not lost, therefore, there was not an actual loss of safety function for the diesel. Corrective actions by the licensee included replacing the fuse and fuse holder and expediting actions to address the extent of condition relative to the as-found condition of the fuse and fuse holder. The finding also affected the cross cutting area of problem identification and resolution since the licensee failed to adequately address the degraded circuit condition in a timely manner. (Section 1R22)


===B.Licensee-Identified Violations===
===Licensee-Identified Violations===


No findings of significance were identified.
No findings of significance were identified.
4


=REPORT DETAILS=
=REPORT DETAILS=
Line 123: Line 71:
===Summary of Plant Status===
===Summary of Plant Status===


The plant operated at approximately 95.5 percent rated thermal power (maintaining 103 percent electrical output) throughout most of the inspection period. On November 18, 2005, reactor
The plant operated at approximately 95.5 percent rated thermal power (maintaining 103 percent electrical output) throughout most of the inspection period. On November 18, 2005, reactor power was reduced to 85 percent to reseat a potentially stuck open moisture separator reheater relief valve. On November 19, 2005, plant operators returned reactor power to 95.5 percent.


power was reduced to 85 percent to reseat a potentially stuck open moisture separator reheater
On December 2, 2005, operators lowered reactor power to 49 percent in response to a ruptured main condenser tube and returned power to 95.5 percent on December 4, 2005. On December 18, 2005, operators lowered reactor power to 90 percent for a planned rod pattern adjustment (All rods out). Power was restored to 95 percent on December 18, 2005, and maintained there through the end of the inspection period.
 
relief valve. On November 19, 2005, plant operators returned reactor power to 95.5 percent.
 
On December 2, 2005, operators lowered reactor power to 49 percent in response to a ruptured
 
main condenser tube and returned power to 95.5 percent on December 4, 2005. On
 
December 18, 2005, operators lowered reactor power to 90 percent for a planned rod pattern
 
adjustment (All rods out). Power was restored to 95 percent on December 18, 2005, and
 
maintained there through the end of the inspection period.1.


==REACTOR SAFETY==
==REACTOR SAFETY==


===Cornerstone: Initiating Events, Mitigating Systems, Barrier Integrity, and Emergency===
===Cornerstone: Initiating Events, Mitigating Systems, Barrier Integrity, and Emergency===


Preparedness1R01Adverse Weather (71111.01)
Preparedness
{{a|1R01}}
==1R01 Adverse Weather==
{{IP sample|IP=IP 71111.01}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the licensee's seasonal readiness preparation checklist for cold weather and to verify that it adequately covered risk-significant equipment and ensured
The inspectors reviewed the licensees seasonal readiness preparation checklist for cold weather and to verify that it adequately covered risk-significant equipment and ensured that the equipment was in a condition to meet the requirements of Technical Specifications (TS), the Operations Requirements Manual (ORM), and the Updated Safety Analysis Report (USAR) with respect to protection from low temperatures. The inspectors verified that minor issues identified during the inspection were entered into the licensees corrective action system by reviewing the associated Condition Reports (CR). The inspectors conducted more detailed system reviews and walkdowns for the reactor core isolation cooling storage tank and service air compressor intake. The inspectors also reviewed several issue reports related to main condenser tube leaks that seem to occur more frequently at the onset of cold weather. These issue reports and other documents reviewed during the inspection are listed at the end of this report. This activity represents one inspection sample.
 
that the equipment was in a condition to meet the requirements of Technical
 
Specifications (TS), the Operations Requirements Manual (ORM), and the Updated Safety Analysis Report (USAR) with respect to protection from low temperatures. The
 
inspectors verified that minor issues identified during the inspection were entered into
 
the licensee's corrective action system by reviewing the associated Condition Reports (CR). The inspectors conducted more detailed system reviews and walkdowns for the
 
reactor core isolation cooling storage tank and service air compressor intake. The
 
inspectors also reviewed several issue reports related to main condenser tube leaks that
 
seem to occur more frequently at the onset of cold weather. These issue reports and
 
other documents reviewed during the inspection are listed at the end of this report. This
 
activity represents one inspection sample.


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified.
 
{{a|1R04}}
51R04Equipment Alignments (71111.04).1Complete Semi-Annual
==1R04 Equipment Alignments==
{{IP sample|IP=IP 71111.04}}
===.1 Complete Semi-Annual===


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors conducted a complete system alignment inspection of the low pressure core spray (LPCS) system. This system was selected based on its high risk significance
The inspectors conducted a complete system alignment inspection of the low pressure core spray (LPCS) system. This system was selected based on its high risk significance and mitigating systems function. The inspectors reviewed plant procedures, drawings, and the USAR to identify proper system alignment and visually inspected system valves, instrumentation, and electrical supplies to verify proper alignment, component accessibility, availability, and current material condition. The inspectors also completed a review of corrective action documents, work orders, and operator work around and challenges to ensure there were no current operability concerns with the system.


and mitigating systems function. The inspectors reviewed plant procedures, drawings, and the USAR to identify proper system alignm ent and visually inspected system valves, instrumentation, and electrical supplies to verify proper alignment, component
Documents reviewed during this inspection are listed in the Attachment. These activities completed one inspection sample.


accessibility, availability, and current material condition. The inspectors also completed
====b. Findings====
 
No findings of significance were identified.
a review of corrective action documents, work orders, and operator work around and
 
challenges to ensure there were no current operability concerns with the system.
 
Documents reviewed during this inspection are listed in the Attachment. These activities


completed one inspection sample.
===.2 Partial Walkdowns===
 
====b. Findings====
No findings of significance were identified..2Partial Walkdowns


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors performed partial walkdowns of accessible portions of divisions of risk-significant mitigating systems equipment during times when the divisions were of
The inspectors performed partial walkdowns of accessible portions of divisions of risk-significant mitigating systems equipment during times when the divisions were of increased importance due to the redundant divisions or other related equipment being unavailable. The inspectors utilized the valve and electric breaker checklists listed in the to verify that the components were properly positioned and that support systems were lined up as needed. The inspectors also examined the material condition of the components and observed operating parameters of equipment to verify that there were no obvious deficiencies. The inspectors reviewed outstanding work orders and CR associated with the divisions to verify that those documents did not reveal issues that could affect division function. The inspectors used the information in the appropriate sections of the USAR to determine the functional requirements of the systems. The documents listed at the end of this report were also used by the inspectors to evaluate this area. The inspectors performed two samples by verifying the alignment of the following divisions:
 
* Auxiliary power system
increased importance due to the redundant divisions or other related equipment being
* Reactor core isolation cooling system
 
unavailable. The inspectors utilized the valve and electric breaker checklists listed in the to verify that the components were properly positioned and that support
 
systems were lined up as needed. The inspectors also examined the material condition
 
of the components and observed operating paramet ers of equipment to verify that there were no obvious deficiencies. The inspectors reviewed outstanding work orders and CR
 
associated with the divisions to verify that those documents did not reveal issues that
 
could affect division function. The inspectors used the information in the appropriate
 
sections of the USAR to determine the functional requirements of the systems. The
 
documents listed at the end of this report were also used by the inspectors to evaluate
 
this area. The inspectors performed two samples by verifying the alignment of the
 
following divisions:*Auxiliary power system*Reactor core isolation cooling system


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified.
 
{{a|1R05}}
61R05Fire Protection (71111.05Q)
==1R05 Fire Protection==
{{IP sample|IP=IP 71111.05Q}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors conducted fire protection walkdowns which were focused on availability, accessibility, and the condition of fire fighting equipment, the control of transient
The inspectors conducted fire protection walkdowns which were focused on availability, accessibility, and the condition of fire fighting equipment, the control of transient combustibles and ignition sources, and on the condition and operating status of installed fire barriers. The inspectors selected fire areas for inspection based on their overall contribution to internal fire risk, as documented in the individual plant examination of external events with later additional insights, their potential to impact equipment which could cause a plant transient, or their impact on the licensees ability to respond to a security event. The inspectors used the documents listed at the end of this report to verify that fire hoses and extinguishers were in their designated locations and available for immediate use, that fire detectors and sprinklers were not obstructed, that transient material loading was within the analyzed limits, and that fire doors, dampers, and penetration seals appeared to be in satisfactory condition. The inspectors verified that minor issues identified during the inspection were entered into the licensees corrective action program.
 
combustibles and ignition sources, and on the condition and operating status of installed
 
fire barriers. The inspectors selected fire areas for inspection based on their overall
 
contribution to internal fire risk, as documented in the individual plant examination of
 
external events with later additional insights, their potential to impact equipment which
 
could cause a plant transient, or their impact on the licensee's ability to respond to a


security event. The inspectors used the documents listed at the end of this report to
The inspectors reviewed portions of the licensees fire protection evaluation report and the USAR to verify consistency in the documented analysis with installed fire protection equipment at the station.


verify that fire hoses and extinguishers were in their designated locations and available
The inspectors completed four samples by inspection of the following areas:
 
C        Fire zone A - 1a: Elevation 707' 6", General Access Area (North)
for immediate use, that fire detectors and sprinklers were not obstructed, that transient
C        Fire zone A - 2a: Elevation 707' 6", RCIC Pump Room C        Fire zone A - 6: Elevation 707' 6", General Access Area (South)
 
C        Fire zone CB-6a: Elevation 800' Main Control Room Complex
material loading was within the analyzed limits, and that fire doors, dampers, and
 
penetration seals appeared to be in satisfactory condition. The inspectors verified that
 
minor issues identified during the inspection were entered into the licensee's corrective
 
action program.
 
The inspectors reviewed portions of the licensee's fire protection evaluation report and the USAR to verify consistency in the docum ented analysis with installed fire protection equipment at the station.
 
The inspectors completed four samples by inspection of the following areas:Fire zone A - 1a: Elevation 707' 6", General Access Area (North)Fire zone A - 2a: Elevation 707' 6", RCIC Pump RoomFire zone A - 6: Elevation 707' 6", General Access Area (South)Fire zone CB-6a: Elevation 800' Main Control Room Complex


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified.
{{a|1R11}}
{{a|1R11}}
==1R11 Licensed Operator Requalification Program (71111.11).1Facility Operating History==
==1R11 Licensed Operator Requalification Program==
{{IP sample|IP=IP 71111.11}}
===.1 Facility Operating History===


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the plant's operating history from January 2004 through October 2005 to assess whether the licensed operator requalification training program
The inspectors reviewed the plants operating history from January 2004 through October 2005 to assess whether the licensed operator requalification training program had identified and addressed operator performance deficiencies at the plant.
 
had identified and addressed operator performance deficiencies at the plant.


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified.


7.2Licensee Requalification Examinations
===.2 Licensee Requalification Examinations===


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors performed a biennial inspection of the licensee's licensed operator requalification training test/examination program. The operating examination material
The inspectors performed a biennial inspection of the licensees licensed operator requalification training test/examination program. The operating examination material reviewed consisted of four operating tests, each containing approximately two dynamic simulator scenarios and approximately five job performance measures. The written examinations reviewed consisted of four written examinations, each containing approximately 35 questions. The inspectors reviewed the annual requalification operating test and biennial written examination material to evaluate general quality, construction, and difficulty level. The inspectors assessed the level of examination material duplication from week-to-week during the current year operating test, and compared the operating test material from this years operating tests (2005) with last years operating tests (2004). The annual operating tests were conducted in September/October/November 2004 and September/October/November 2005. The examiners assessed the amount of written examination material duplication from week-to-week for the written examination administered in September/October/November 2005. The inspectors reviewed the methodology for developing the examinations, including the licensed operator requalification training program two year sample plan, probabilistic risk assessment insights, previously identified operator performance deficiencies, and plant modifications.


reviewed consisted of four operating tests, each containing approximately two dynamic
====b. Findings====
No findings of significance were identified.


simulator scenarios and approximately five job performance measures. The written
===.3 Licensee Administration of Requalification Examinations===


examinations reviewed consisted of four written examinations, each containing
====a. Inspection Scope====
The inspectors observed the administration of a requalification operating test to assess the licensees effectiveness in conducting the test. The inspectors evaluated the performance of one shift crew in parallel with the facility evaluators during two dynamic simulator scenarios and evaluated various licensed crew members concurrently with facility evaluators during the administration of several job performance measures. The inspectors assessed the facility evaluators ability to determine adequate crew and individual performance using objective, measurable standards. The inspectors observed the training staff personnel administer the operating test, including conducting pre-examination briefings, evaluations of operator performance, and individual and crew evaluations upon completion of the operating test. The inspectors evaluated the ability of the simulator to support the examinations. A specific evaluation of simulator performance was conducted and documented under Section 1R11.9, Conformance With Simulator Requirements Specified in 10 CFR 55.46, of this report.


approximately 35 questions. The inspectors reviewed the annual requalification
====b. Findings====
No findings of significance were identified.


operating test and biennial written examination material to evaluate general quality, construction, and difficulty level. The inspectors assessed the level of examination
===.4 Examination Security===


material duplication from week-to-week during the current year operating test, and
====a. Inspection Scope====
The inspectors observed and reviewed the licensees overall licensed operator requalification examination security program related to examination physical security (e.g., access restrictions and simulator considerations) and integrity (e.g., predictability and bias). The inspectors also reviewed the facility licensees examination security procedure, any corrective actions related to past or present examination security problems at the facility, and the implementation of security and integrity measures (e.g., security agreements, sampling criteria, bank use, and test item repetition)throughout the examination process.


compared the operating test material from this year's operating tests (2005) with last
====b. Findings====
No findings of significance were identified.


year's operating tests (2004). The annual operating tests were conducted in
===.5 Licensee Training Feedback System===
 
September/October/November 2004 and S eptember/October/November 2005. The examiners assessed the amount of writt en examination material duplication from week-to-week for the written examination administered in
 
September/October/November 2005. The ins pectors reviewed the methodology for developing the examinations, including the licensed operator requalification training
 
program two year sample plan, probabilis tic risk assessment insights, previously identified operator performance deficiencies, and plant modifications.
 
====b. Findings====
No findings of significance were identified..3Licensee Administration of Requalification Examinations


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors observed the administration of a requalification operating test to assess the licensee's effectiveness in conducting the test. The inspectors evaluated the
The inspectors assessed the methods and effectiveness of the licensees processes for revising and maintaining its licensed operator requalification training program up to date, including the use of feedback from plant events and industry experience information.
 
performance of one shift crew in parallel wi th the facility evaluators during two dynamic simulator scenarios and evaluated various licensed crew members concurrently with
 
facility evaluators during the administration of several job performance measures. The
 
inspectors assessed the facility evaluators' ability to determine adequate crew and
 
individual performance using objective, meas urable standards. The inspectors observed the training staff personnel administer the operating test, including conducting
 
pre-examination briefings, evaluations of operator performance, and individual and crew


evaluations upon completion of the operating test. The inspectors evaluated the ability
The inspectors reviewed the licensees quality assurance oversight activities, including licensee training department self-assessment reports. The inspectors evaluated the licensees ability to assess the effectiveness of its licensed operator requalification training program and the licensees ability to implement appropriate corrective actions.
 
of the simulator to support the examinations. A specific evaluation of simulator
 
performance was conducted and documented under Section 1R11.9, "Conformance
 
With Simulator Requirements Specified in 10 CFR 55.46," of this report.


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified.


8.4Examination Security
===.6 Licensee Remedial Training Program===


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors observed and reviewed the licensee's overall licensed operator requalification examination security program related to examination physical security (e.g., access restrictions and simulator considerations) and integrity (e.g., predictability
The inspectors assessed the adequacy and effectiveness of the remedial training conducted since the previous biennial requalification examinations and the training planned for the current examination cycle to ensure that the licensee addressed weaknesses in licensed operator or crew performance identified during training and plant operations. The inspectors reviewed remedial training procedures and individual remedial training plans.
 
and bias). The inspectors also reviewed the facility licensee's examination security
 
procedure, any corrective actions related to past or present examination security
 
problems at the facility, and the implementation of security and integrity measures (e.g., security agreements, sampling criteria, bank use, and test item repetition)
 
throughout the examination process.


====b. Findings====
====b. Findings====
No findings of significance were identified..5Licensee Training Feedback System
No findings of significance were identified.


====a. Inspection Scope====
===.7 Conformance With Operator License Conditions===
The inspectors assessed the methods and effectiveness of the licensee's processes for revising and maintaining its licensed operator requalification training program up to date, including the use of feedback from plant events and industry experience information.
 
The inspectors reviewed the licensee's quality assurance oversight activities, including
 
licensee training department self-assessment reports. The inspectors evaluated the
 
licensee's ability to assess the effectiveness of its licensed operator requalification
 
training program and the licensee's ability to implement appropriate corrective actions.
 
====b. Findings====
No findings of significance were identified..6Licensee Remedial Training Program


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors assessed the adequacy and effectiveness of the remedial training conducted since the previous biennial requalification examinations and the training
The inspectors reviewed the facility and individual operator licensees' conformance with the requirements of 10 CFR Part 55. The inspectors reviewed the facility licensee's program for maintaining active operator licenses and to assess compliance with 10 CFR 55.53
: (e) and (f). The inspectors reviewed the procedural guidance and the process for tracking on-shift hours for licensed operators and which control room positions were granted watch-standing credit for maintaining active operator licenses.


planned for the current examination cycle to ensure that the licensee addressed
The inspectors reviewed the facility licensee's licensed operator requalification training program to assess compliance with the requalification program requirements as described by 10 CFR 55.59 (c). Additionally, medical records for 16 licensed operators were reviewed for compliance with 10 CFR 55.53 (i).
 
weaknesses in licensed operator or crew performance identified during training and
 
plant operations. The inspectors reviewed remedial training procedures and individual
 
remedial training plans.


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified.


9.7Conformance With Operator License Conditions
===.8 Annual Operating Test Results===


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the facility and individual operator licensees' conformance with the requirements of 10 CFR Part 55. The inspectors reviewed the facility licensee's
The inspector reviewed the overall pass/fail results of the annual operating examination which consisted of job performance measure and simulator operating tests (required per 10 CFR 55.59(a)(2)) administered by the licensee. The inspectors reviewed the overall pass/fail results for the biennial written examination (required per 10 CFR 55.59(a)(2))
 
administered by the licensee. The overall results were compared with the significance determination process in accordance with NRC Manual Chapter 0609I, Operator Requalification Human Performance Significance Determination Process (SDP). This represented one sample.
program for maintaining active operator licenses and to assess compliance with
 
10 CFR 55.53
: (e) and (f). The inspectors reviewed the procedural guidance and the
 
process for tracking on-shift hours for licensed operators and which control room
 
positions were granted watch-standing credit for maintaining active operator licenses.
 
The inspectors reviewed the facility licensee's licensed operator requalification training
 
program to assess compliance with the requalification program requirements as
 
described by 10 CFR 55.59 (c). Additionally, medical records for 16 licensed operators
 
were reviewed for compliance with 10 CFR 55.53 (i).


====b. Findings====
====b. Findings====
No findings of significance were identified..8Annual Operating Test Results
No findings of significance were identified.


====a. Inspection Scope====
===.9 Conformance With Simulator Requirements Specified in 10 CFR 55.46===
The inspector reviewed the overall pass/fail results of the annual operating examination which consisted of job performance measure and simulator operating tests (required per
 
10 CFR 55.59(a)(2)) administered by the licensee. The inspectors reviewed the overall
 
pass/fail results for the biennial written examination (required per 10 CFR 55.59(a)(2))
 
administered by the licensee. The overall results were compared with the significance
 
determination process in accordance with NRC Manual Chapter 0609I, "Operator
 
Requalification Human Performance Significance Determination Process (SDP)."  This
 
represented one sample.
 
====b. Findings====
No findings of significance were identified..9Conformance With Simulator Requirements Specified in 10 CFR 55.46


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors assessed the adequacy of the licensee's simulation facility (simulator) for use in operator licensing examinations and for satisfying experience requirements as
The inspectors assessed the adequacy of the licensees simulation facility (simulator) for use in operator licensing examinations and for satisfying experience requirements as prescribed in 10 CFR 55.46, Simulation Facilities. The inspectors also reviewed a sample of simulator performance test records (i.e., transient tests, scenario test and discrepancy resolution validation test), simulator discrepancy and modification records, and the process for ensuring continued assurance of simulator fidelity in accordance with 10 CFR 55.46. The inspectors reviewed and evaluated the discrepancy process to ensure that simulator fidelity was maintained. Open simulator discrepancies were reviewed for importance relative to the impact on 10 CFR 55.45 and 55.59 operator actions as well as on nuclear and thermal hydraulic operating characteristics. The inspectors conducted interviews with members of the licensees simulator staff about the configuration control process and completed the IP 71111.11, Appendix C, checklist to evaluate whether or not the licensees plant-referenced simulator was operating adequately as required by 10 CFR 55.46
 
prescribed in 10 CFR 55.46, "Simulation Facilities.The inspectors also reviewed a
 
sample of simulator performance test records (i.e., transient tests, scenario test and
 
discrepancy resolution validation test), simulator discrepancy and modification records, and the process for ensuring continued assurance of simulator fidelity in accordance
 
with 10 CFR 55.46. The inspectors reviewed and evaluated the discrepancy process to
 
ensure that simulator fidelity was maintained. Open simulator discrepancies were
 
reviewed for importance relative to the impact on 10 CFR 55.45 and 55.59 operator 10 actions as well as on nuclear and thermal hydraulic operating characteristics. The inspectors conducted interviews with members of the licensee's simulator staff about the
 
configuration control process and completed the IP 71111.11, Appendix C, checklist to
 
evaluate whether or not the licensee's plant-referenced simulator was operating
 
adequately as required by 10 CFR 55.46
: (c) and (d).
: (c) and (d).


====b. Findings====
====b. Findings====
No findings of significance were identified..10Quarterly Resident Inspector Review
No findings of significance were identified.
 
===.10 Quarterly Resident Inspector Review===


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed licensed-operator requalification training to evaluate operator performance in mitigating the consequences of a simulated event, particularly in the
The inspectors reviewed licensed-operator requalification training to evaluate operator performance in mitigating the consequences of a simulated event, particularly in the areas of human performance. The inspectors evaluated operator performance attributes which included communication clarity and formality, timely performance of appropriate operator actions, appropriate alarm response, proper procedure use and adherence, and senior reactor operator oversight and command and control.
 
areas of human performance. The inspectors evaluated operator performance attributes
 
which included communication clarity and formality, timely performance of appropriate
 
operator actions, appropriate alarm response, proper procedure use and adherence, and
 
senior reactor operator oversight and command and control.
 
Crew performance in these areas was compared to licensee management expectations and guidelines as presented in the following documents:*ESG-LOR-85 - "Loss of 6.9 kV Bus 1B, ATWS - Drywell Leak"*ESG-LOR-74 - "Steam Leak, Drywell Leak, Figure N Blowdown"
*OP-AA-101-111, "Roles and Responsibilities of On-shift Personnel," Rev 0
*OP-AA-103-102, "Watchstanding Practices," Rev 2
*OP-AA-104-101, "Communications," Rev 1
*OP-AA-106-101, "Significant Event Reporting," Rev 2 The inspectors also assessed the performance of the training staff evaluators involved in the requalification process. For any weaknesses identified, the inspectors observed that


the licensee evaluators also noted the issues and discussed them in the critique at the
Crew performance in these areas was compared to licensee management expectations and guidelines as presented in the following documents:
 
* ESG-LOR-85 - Loss of 6.9 kV Bus 1B, ATWS - Drywell Leak
end of the session. The inspectors verified all issues were captured in the training
* ESG-LOR-74 - Steam Leak, Drywell Leak, Figure N Blowdown
 
* OP-AA-101-111, Roles and Responsibilities of On-shift Personnel, Rev 0
program and licensee corrective action process.
* OP-AA-103-102, Watchstanding Practices, Rev 2
* OP-AA-104-101, Communications, Rev 1
* OP-AA-106-101, Significant Event Reporting, Rev 2 The inspectors also assessed the performance of the training staff evaluators involved in the requalification process. For any weaknesses identified, the inspectors observed that the licensee evaluators also noted the issues and discussed them in the critique at the end of the session. The inspectors verified all issues were captured in the training program and licensee corrective action process.


These activities completed two inspection samples.
These activities completed two inspection samples.
Line 455: Line 227:
No findings of significance were identified.
No findings of significance were identified.
{{a|1R12}}
{{a|1R12}}
==1R12 Maintenance Effectiveness (71111.12Q)==
==1R12 Maintenance Effectiveness==
{{IP sample|IP=IP 71111.12Q}}
The inspectors reviewed the effectiveness of the licensees maintenance efforts in implementing the Maintenance Rule (MR) requirements, including a review of scoping, goal-setting, performance monitoring, short and long-term corrective actions, and current equipment performance problems. Systems were selected based on their designation as risk significant under the maintenance rule, or being in the increased monitoring (MR category (a) (1)) group. In addition, the inspectors interviewed the system engineers and maintenance rule coordinator. The inspectors also reviewed condition reports and associated documents for appropriate identification of problems, entry into the corrective action system, and appropriateness of planned or completed actions. The documents reviewed are listed at the end of the report. The inspectors completed two samples by reviewing the following:
* Reactor protection system
* Containment ventilation system and continuous containment purge system


The inspectors reviewed the effectiveness of the licensee's maintenance efforts in implementing the Maintenance Rule (MR) requirements, including a review of scoping, goal-setting, performance monitoring, short and long-term corrective actions, and current
====b. Findings====
 
No findings of significance were identified.
equipment performance problems. Systems were selected based on their designation 11 as risk significant under the maintenance rule, or being in the increased monitoring (MR category (a) (1)) group. In addition, the inspectors interviewed the system engineers
 
and maintenance rule coordinator. The inspectors also reviewed condition reports and
 
associated documents for appropriate identification of problems, entry into the corrective
 
action system, and appropriateness of planned or completed actions. The documents
 
reviewed are listed at the end of the report. The inspectors completed two samples by
 
reviewing the following:*Reactor protection system*Containment ventilation system and continuous containment purge systemb.Findings No findings of significance were identified.
{{a|1R13}}
{{a|1R13}}
==1R13 Maintenance Risk Assessment (71111.13)==
==1R13 Maintenance Risk Assessment==
{{IP sample|IP=IP 71111.13}}
The inspectors observed the licensees risk assessment processes and considerations used to plan and schedule maintenance activities on safety-related structures, systems, and components, particularly to ensure that maintenance risk and emergent work contingencies had been identified and resolved. The inspectors completed five samples by assessing the effectiveness of risk management activities for the following work activities or work weeks:
* Emergency reserve auxiliary transformer system outage
* Standby liquid control (both trains) inoperable due to the performance of limit switch maintenance on 1C41-F031 (WO# 668279)
* Division I diesel generator ventilation fan control in pull-to-lock to support troubleshooting activities concurrent with planned maintenance on division 1 essential switchgear heat removal (WR# 189992)
* Cumulative review of licensee risk management assessments following transfer of 1B1 Bus to the reserve auxiliary transformer and then back to the emergency reserve auxiliary transformer for post maintenance test on 1AP09EC synch check relay as directed by WO# 758834-02, division II standby gas treatment system out of service for planned maintenance, and division II essential switchgear heat removal fan and chiller out of service for planned maintenance
* Licensee risk assessment activities and redundant system protection activities following a trip of the division III diesel during a monthly run


The inspectors observed the licensee's risk assessment processes and considerations used to plan and schedule maintenance activities on safety-related structures, systems, and components, particularly to ensure that maintenance risk and emergent work
====b. Findings====
 
No findings of significance were identified.
contingencies had been identified and resolved. The inspectors completed five samples
 
by assessing the effectiveness of risk management activities for the following work
 
activities or work weeks:*Emergency reserve auxiliary transformer system outage*Standby liquid control (both trains) inoperable due to the performance of limit switch maintenance on 1C41-F031 (WO# 668279)*Division I diesel generator ventilation fan control in pull-to-lock to support troubleshooting activities concurrent with planned maintenance on division 1
 
essential switchgear heat removal (WR# 189992)*Cumulative review of licensee risk management assessments following transfer of 1B1 Bus to the reserve auxiliary tr ansformer and then back to the emergency reserve auxiliary transformer for pos t maintenance test on 1AP09EC synch check relay as directed by WO# 758834-02, division II standby gas treatment
 
system out of service for planned maintenance, and division II essential
 
switchgear heat removal fan and chiller out of service for planned maintenance*Licensee risk assessment activities and redundant system protection activities following a trip of the division III diesel during a monthly runb.Findings No findings of significance were identified.
{{a|1R14}}
{{a|1R14}}
==1R14 Non-routine Evolutions (71111.14)==
==1R14 Non-routine Evolutions==
{{IP sample|IP=IP 71111.14}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed personnel performance during planned and unplanned plant evolutions and selected licensee event reports focusing on those involving personnel 12 response to non-routine conditions. The review was performed to ascertain that operator responses were in accordance with the required procedures. In particular, the
The inspectors reviewed personnel performance during planned and unplanned plant evolutions and selected licensee event reports focusing on those involving personnel response to non-routine conditions. The review was performed to ascertain that operator responses were in accordance with the required procedures. In particular, the inspectors completed one sample by reviewing personnel performance during the following plant event:
 
* Plant Operations activities in response to main condenser tube failure
inspectors completed one sample by reviewing personnel performance during the
 
following plant event:*Plant Operations activities in response to main condenser tube failure


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified.
{{a|1R15}}
{{a|1R15}}
==1R15 Operability Evaluations (71111.15)==
==1R15 Operability Evaluations==
{{IP sample|IP=IP 71111.15}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the following operability determinations and evaluations affecting mitigating systems to determine whether operability was properly justified and
The inspectors reviewed the following operability determinations and evaluations affecting mitigating systems to determine whether operability was properly justified and the component or system remained available such that no unrecognized risk increase had occurred. The inspectors completed three samples of operability determinations and evaluations by reviewing the following:
 
* Division II diesel generator - failure of division II DC oil pumps to keep running due to a high current overload on F5-1 fuse
the component or system remained available such that no unrecognized risk increase
* Reactor core isolation cooling tank vortex issue
 
* High pressure core spray suppression pool suction valve
had occurred. The inspectors completed three samples of operability determinations
 
and evaluations by reviewing the following:*Division II diesel generator - failure of division II DC oil pumps to keep running due to a high current overload on F5-1 fuse*Reactor core isolation cooling tank vortex issue
*High pressure core spray suppression pool suction valve


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified.
{{a|1R16}}
{{a|1R16}}
==1R16 Operator Workarounds (71111.16)==
==1R16 Operator Workarounds==
 
{{IP sample|IP=IP 71111.16}}
===.1 Review of selected workaround issue===
===.1 Review of selected workaround issue===


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors assessed the following operator workaround issue to determine the potential effects on the functionality of the corresponding system:*Condensate pump suction pressure - condensate pump suction pressure is degraded During this inspection, the inspectors reviewed the technical adequacy of the workaround documentation against the updated safety analysis report and other design
The inspectors assessed the following operator workaround issue to determine the potential effects on the functionality of the corresponding system:
* Condensate pump suction pressure - condensate pump suction pressure is degraded During this inspection, the inspectors reviewed the technical adequacy of the workaround documentation against the updated safety analysis report and other design information to assess whether the workaround conflicted with any design basis information. The inspectors compared the information in abnormal or emergency operating procedures to the workaround information to ensure that the operators maintained the ability to implement important procedures when needed.


information to assess whether the workaround conflicted with any design basis
This represented one inspection sample.


information. The inspectors compared the information in abnormal or emergency
====b. Findings====
No findings of significance were identified.


operating procedures to the workaround information to ensure that the operators
===.2 Semi-annual Review of the Cumulative Effects of Operator Workarounds===
 
maintained the ability to implement important procedures when needed.
 
13 This represented one inspection sample.
 
====b. Findings====
No findings of significance were identified..2Semi-annual Review of the Cumulative Effects of Operator Workarounds


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed all operator workarounds and challenges to identify any potential effect on mitigating systems ability to function as required during emergencies
The inspectors reviewed all operator workarounds and challenges to identify any potential effect on mitigating systems ability to function as required during emergencies and ensure that operators would be able to respond in a correct and timely manner to plant transients and accidents. The inspectors utilized procedure OP-AA-102-103, Operator Work-Around Program, revision 1, during the review. The inspectors also reviewed issue reports and work orders related to corrective actions to remove the workarounds or compensatory actions.


and ensure that operators would be able to respond in a correct and timely manner to
The inspectors completed one sample by reviewing the following workarounds and challenges:
 
* N66-D006B off gas regenerator dryer thermostatic trap
plant transients and accidents. The inspectors utilized procedure OP-AA-102-103, "Operator Work-Around Program," revision 1, during the review. The inspectors also
* 1FW01 PB turbine-driven reactor feed pump 1B
 
* 1WS026 turbine oil cooler temperature control valve
reviewed issue reports and work orders related to corrective actions to remove the
* Condensate pump suction pressure
 
* 1G33-D001 reactor water cleanup orifice letdown to main condenser
workarounds or compensatory actions.
* Modification to improve feedwater system control post scram
 
* 1B21-F437A steam jet air ejector 1A steam inlet control valve bypass
The inspectors completed one sample by reviewing the following workarounds and challenges: *N66-D006B off gas regenerator dryer thermostatic trap*1FW01 PB turbine-driven reactor feed pump 1B  
* 0WE01FA (B) [C] radwaste filters A (B) [C]
*1WS026 turbine oil cooler temperature control valve
*Condensate pump suction pressure
*1G33-D001 reactor water cleanup orifice letdown to main condenser
*Modification to improve feedwater system control post scram
*1B21-F437A steam jet air ejector 1A steam inlet control valve bypass
*0WE01FA (B) [C] radwaste filters A (B) [C]


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified.
{{a|1R19}}
{{a|1R19}}
==1R19 Post Maintenance Testing (71111.19)==
==1R19 Post Maintenance Testing==
{{IP sample|IP=IP 71111.19}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the post maintenance testing activities associated with maintenance or modification of important mitigating, barrier integrity, and support
The inspectors reviewed the post maintenance testing activities associated with maintenance or modification of important mitigating, barrier integrity, and support systems that were identified as risk significant in the licensees risk analysis. The inspectors reviewed these activities to verify that the post maintenance testing was performed adequately, demonstrated that the maintenance was successful, and that operability was restored. During this inspection activity, the inspectors interviewed maintenance and engineering department personnel and reviewed the completed post maintenance testing documentation. The inspectors used the appropriate sections of the TS and USAR, as well as the documents listed at the end of this report, to evaluate this area.


systems that were identified as risk significant in the licensee's risk analysis. The
Testing subsequent to the following activities was observed and evaluated to complete seven inspection samples:
 
* Reviewed completed CPS 3412.01, Essential switchgear heat removal, following completion of WO# 752802, 1SX202A relief valve and 1SX110BA pipe replacement
inspectors reviewed these activities to ve rify that the post maintenance testing was performed adequately, demonstrated that the maintenance was successful, and that
* Electrical Maintenance troubleshoot/rework/adjust to restore sat operation, standby liquid control test tank outlet valve limit switch WO# 668279
 
* Standby Gas Treatment Train B - containment draw down test following work to correct flow oscillations WO# 657204, OP 9065.02 OP secondary containment integrity; January 18, 2004, and WO# 655681, IM Flow indication oscillating
operability was restored. During this inspection activity, the inspectors interviewed
          +/- 400 scfm; November 22, 2005
 
* Division III diesel generator high water temperature switch replacement
maintenance and engineering department personnel and reviewed the completed post
* Reviewed Section 8.14.18 of CPS 9061.06C014 to ensure post maintenance testing adequacy following removal of deluge line flange and reinstallation of spool piece for 1SX073B standby gas treatment 1B deluge valve
 
* Reviewed CPS 3412.01, Essential switchgear heat removal, following completion of WO #616616, circuit breaker and bucket replacement
maintenance testing documentation. The inspectors used the appropriate sections of
* Reviewed results of CPS 8731.12 following rod control and information system transponder card replacement WO# 647415
 
the TS and USAR, as well as the documents listed at the end of this report, to evaluate
 
this area.
 
14 Testing subsequent to the following activities was observed and evaluated to complete seven inspection samples:*Reviewed completed CPS 3412.01, Essential switchgear heat removal, followingcompletion of WO# 752802, 1SX202A relief valve and 1SX110BA pipe
 
replacement*Electrical Maintenance troubleshoot/rework/adjust to restore sat operation, standby liquid control test tank outlet valve limit switch WO# 668279*Standby Gas Treatment Train B - containment draw down test following work to correct flow oscillations WO# 657204, OP 9065.02 OP secondary containment
 
integrity; January 18, 2004, and WO# 655681, IM Flow indication oscillating
 
+/- 400 scfm; November 22, 2005*Division III diesel generator high water temperature switch replacement
*Reviewed Section 8.14.18 of CPS 9061.06C014 to ensure post maintenance testing adequacy following removal of deluge line flange and reinstallation of spool piece for 1SX073B standby gas treatment 1B deluge valve*Reviewed CPS 3412.01, Essential switchgear heat removal, following completion of WO #616616, circuit breaker and bucket replacement*Reviewed results of CPS 8731.12 following rod control and information system transponder card replacement WO# 647415


====b. Findings====
====b. Findings====
Introduction
:  A self-revealing Green finding involving a non-cited violation (NCV) of Technical Specification 5.4 "Procedures," was identified. On September 30, 2005, the
Division III emergency diesel generator (EDG) failed to properly run following
maintenance activities, due to inadequate maintenance instructions. The licensee
determined that this issue was the result of a maintenance planner's failure to follow
administrative guidelines for technical review during the development of the
maintenance instructions. This issue resulted in extended outage and unavailability time
of the EDG.
Discussion
:  On September 30, 2005, the Division III EDG was started for a maintenance run following a system outage window. During the initial start of the EDG, the start sequence was normal. Followup adjustments were then made on a newly
installed shutdown solenoid. The licensee's operations staff declared the diesel
generator available if needed to response to an event. The licensee's online risk profile
changed from "Yellow" to "Green."  At this time compensatory actions such as the
establishment of protected system pathways were removed.
During subsequent starts, the EDG exhibited abnormal starting indication. While starting the EDG for post maintenance test, the licensee observed a starting time of greater than
12 seconds. Additionally, unusual speed and voltage variations occurred when
operators made adjustments to the diesel voltage regulator while the diesel was running.
A licensee investigation determined that due to a lack of technical rigor for EDG shutdown solenoid and servo booster replacement, the work instructions performing
these tasks contained inadequate guidance which allowed air to be trapped in the servo 15 booster motor. The servo booster motor is a part of the governor. The air trapped on the oil side of the governor's operating piston resulted in the governor not being able to
perform its designed function. This issue resulted in lengthening the time in which the
Division III EDG was unavailable and inoperable.
The licensee's investigation also determined that the work instructions failed to contain adequate instructions for venting or draining air from the governor following the
replacement of the servo booster. The licensee concluded that this issue would not


have occurred if the work planner responsible for the work instructions would have
=====Introduction:=====
A self-revealing Green finding involving a non-cited violation (NCV) of Technical Specification 5.4 Procedures, was identified. On September 30, 2005, the Division III emergency diesel generator (EDG) failed to properly run following maintenance activities, due to inadequate maintenance instructions. The licensee determined that this issue was the result of a maintenance planners failure to follow administrative guidelines for technical review during the development of the maintenance instructions. This issue resulted in extended outage and unavailability time of the EDG.


contacted the appropriate engineering staff per the licensee's "Performance Centered
Discussion: On September 30, 2005, the Division III EDG was started for a maintenance run following a system outage window. During the initial start of the EDG, the start sequence was normal. Followup adjustments were then made on a newly installed shutdown solenoid. The licensees operations staff declared the diesel generator available if needed to response to an event. The licensees online risk profile changed from Yellow to Green. At this time compensatory actions such as the establishment of protected system pathways were removed.


Maintenance" (MA-AA-716-210) procedure. This procedure required the maintenance
During subsequent starts, the EDG exhibited abnormal starting indication. While starting the EDG for post maintenance test, the licensee observed a starting time of greater than 12 seconds. Additionally, unusual speed and voltage variations occurred when operators made adjustments to the diesel voltage regulator while the diesel was running.


planner to route the work instructions to the licensee's engineering staff for a formal
A licensee investigation determined that due to a lack of technical rigor for EDG shutdown solenoid and servo booster replacement, the work instructions performing these tasks contained inadequate guidance which allowed air to be trapped in the servo booster motor. The servo booster motor is a part of the governor. The air trapped on the oil side of the governors operating piston resulted in the governor not being able to perform its designed function. This issue resulted in lengthening the time in which the Division III EDG was unavailable and inoperable.


review of technical information.
The licensees investigation also determined that the work instructions failed to contain adequate instructions for venting or draining air from the governor following the replacement of the servo booster. The licensee concluded that this issue would not have occurred if the work planner responsible for the work instructions would have contacted the appropriate engineering staff per the licensees Performance Centered Maintenance (MA-AA-716-210) procedure. This procedure required the maintenance planner to route the work instructions to the licensees engineering staff for a formal review of technical information.


=====Analysis:=====
=====Analysis:=====
Failure to provide adequate maintenance and work instruction is a performance deficiency. The inspectors compared this finding to the findings identified
Failure to provide adequate maintenance and work instruction is a performance deficiency. The inspectors compared this finding to the findings identified in Appendix E, Examples of Minor Issues, of IMC 0612, Power Reactor Inspection Reports, dated September 30, 2005, to determine whether the finding was minor. The inspectors determined that no example contained in Appendix E was applicable to this situation. The inspectors then reviewed this finding against the guidance contained in Appendix B, Issue Dispositioning Screening, of IMC 0612. The inspectors determined that despite the fact that this issue involved work in progress, this issue was more than minor because the finding affected the Mitigating Systems Cornerstone objective of ensuring the availability of mitigating systems to prevent undesirable consequences.
 
in Appendix E, "Examples of Minor Issues," of IMC 0612, "Power Reactor Inspection
 
Reports," dated September 30, 2005, to determine whether the finding was minor. The
 
inspectors determined that no example contained in Appendix E was applicable to this
 
situation. The inspectors then reviewed this finding against the guidance contained in
 
Appendix B, "Issue Dispositioning Screening," of IMC 0612. The inspectors determined
 
that despite the fact that this issue involved work in progress, this issue was more than
 
minor because the finding affected the Mitigating Systems Cornerstone objective of
 
ensuring the availability of mitigating systems to prevent undesirable consequences.
 
The issue resulted in the emergency diesel generator being unavailable for longer than
 
expected by the plant staff. Following the initial maintenance run of the diesel generator
 
operators declared that the diesel generator was available for use, if needed to respond
 
to an event. At this time, a number of compensatory actions such as the establishment
 
of protected system pathways were eliminated. The inspectors completed a Phase 1


significance determination of this issue using IMC 0609, "Significance Determination
The issue resulted in the emergency diesel generator being unavailable for longer than expected by the plant staff. Following the initial maintenance run of the diesel generator operators declared that the diesel generator was available for use, if needed to respond to an event. At this time, a number of compensatory actions such as the establishment of protected system pathways were eliminated. The inspectors completed a Phase 1 significance determination of this issue using IMC 0609, Significance Determination Process, Appendix A, Attachment 1, dated November 22, 2005. The inspectors selected the Mitigating Systems Cornerstone. The inspectors answered no to all five questions. Therefore, the inspectors concluded that this issue was a finding of very low safety significance (Green).
 
Process," Appendix A, Attachment 1, dated November 22, 2005. The inspectors
 
selected the Mitigating Systems Cornerstone. The inspectors answered "no" to all five
 
questions. Therefore, the inspectors concluded that this issue was a finding of very low
 
safety significance (Green).


=====Enforcement:=====
=====Enforcement:=====
Technical Specification 5.4.1, states that written procedures shall be established, implemented, and maintained covering the applicable procedures
Technical Specification 5.4.1, states that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.
 
recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.
 
Appendix A of Regulatory Guide 1.33, recommends that procedures for performing
 
maintenance that can affect the performance of safety-related equipment should be
 
properly preplanned and performed in accordance with written procedures, documented
 
instructions, or drawings appropriate to the circumstances.
 
Contrary to the above, the licensee's procedures for performing maintenance on the Division III EDG were inadequate, in that, the work instruction did not prevent air from
 
being trapped in the servo booster motor and did not vent the air following the servo
 
booster replacement. On September 30, 2005, the licensee's failure to have adequate
 
maintenance procedures resulted in the diesel generator not operating properly. This


was a violation. Corrective actions by the licensee included developing lesson-learned 16 information so issues surrounding this finding would be shared with other licensee staff.
Appendix A of Regulatory Guide 1.33, recommends that procedures for performing maintenance that can affect the performance of safety-related equipment should be properly preplanned and performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances.


Additionally, the licensee planned to add technical guidance related to venting air from
Contrary to the above, the licensees procedures for performing maintenance on the Division III EDG were inadequate, in that, the work instruction did not prevent air from being trapped in the servo booster motor and did not vent the air following the servo booster replacement. On September 30, 2005, the licensees failure to have adequate maintenance procedures resulted in the diesel generator not operating properly. This was a violation. Corrective actions by the licensee included developing lesson-learned information so issues surrounding this finding would be shared with other licensee staff.


the diesel governor to the licensee's diesel maintenance training material.
Additionally, the licensee planned to add technical guidance related to venting air from the diesel governor to the licensees diesel maintenance training material.


The finding also affected the cross cutting area of human performance since the licensee's maintenance personnel failed to request formal technical guidance from
The finding also affected the cross cutting area of human performance since the licensees maintenance personnel failed to request formal technical guidance from engineering staff as directed by licensee administrative procedures. Because the finding has been captured by the licensees corrective action program (CR 379980), this violation is being treated as a non-cited violation (NCV 05000461/200509-01(DRP))
 
engineering staff as directed by licensee administrative procedures. Because the finding
 
has been captured by the licensee's corrective action program (CR 379980), this violation is being treated as a non-cited violation (NCV 05000461/200509-01(DRP))
consistent with Section VI.A.1 of the NRC Enforcement Policy.
consistent with Section VI.A.1 of the NRC Enforcement Policy.
{{a|1R22}}
{{a|1R22}}
==1R22 Surveillance Testing (71111.22)==
==1R22 Surveillance Testing==
{{IP sample|IP=IP 71111.22}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors witnessed selected surveillance testing and/or reviewed test data to verify that the equipment tested using the surveillance procedures met the TS, the ORM, the USAR, and licensee procedural requirements, and demonstrated that the equipment
The inspectors witnessed selected surveillance testing and/or reviewed test data to verify that the equipment tested using the surveillance procedures met the TS, the ORM, the USAR, and licensee procedural requirements, and demonstrated that the equipment was capable of performing its intended safety functions. The activities were selected based on their importance in verifying mitigating systems capability and barrier integrity.


was capable of performing its intended safety functions. The activities were selected
The inspectors used the documents listed at the end of this report to verify that the testing met the frequency requirements; that the tests were conducted in accordance with the procedures, including establishing the proper plant conditions and prerequisites; that the test acceptance criteria were met; and that the results of the tests were properly reviewed and recorded. In addition, the inspectors interviewed operations, maintenance and engineering department personnel regarding the tests and test results.


based on their importance in verifying mitigating systems capability and barrier integrity.
The inspectors evaluated the following surveillance tests to complete six inspection samples:
 
* CPS 9051.02 High Pressure Core Spray Valve Operability Surveillance
The inspectors used the documents listed at the end of this report to verify that the
* CPS 9431.04C20, Reactor Protection System Reactor Water Level WO # 686384-01
 
* CPS 9057.02 Secondary Containment Integrity
testing met the frequency requirements; that the tests were conducted in accordance
* CPS 9053.01C001 Residual Heat Removal Loop A Valve Operability
 
* CPS 9080.02 Diesel Generator 1B Operability - Manual Quick Start Operability
with the procedures, including establishing the proper plant conditions and prerequisites;
* CPS 9080.03 Diesel Generator 1C Operability - Manual Quick Start Operability
 
that the test acceptance criteria were met; and that the results of the tests were properly
 
reviewed and recorded. In addition, the inspectors interviewed operations, maintenance
 
and engineering department personnel regarding the tests and test results.
 
The inspectors evaluated the following surveillance tests to complete six inspectionsamples:*CPS 9051.02 "High Pressure Core Spray Valve Operability Surveillance"*CPS 9431.04C20, "Reactor Protection System Reactor Water Level" WO # 686384-01*CPS 9057.02 "Secondary Containment Integrity"
*CPS 9053.01C001 "Residual Heat Removal Loop A Valve Operability"
*CPS 9080.02 "Diesel Generator 1B Operability - Manual Quick Start Operability"
*CPS 9080.03 "Diesel Generator 1C Operability - Manual Quick Start Operability"


====b. Findings====
====b. Findings====
Introduction
:  The inspectors identified a Green finding involving a non-cited violation for inadequate corrective action. The licensee's failure to properly identify and correct a
degraded electrical circuit in 2004, resulted in the Division II EDG subsystem being
vulnerable to electrical circuit failure if called upon to complete its support function. This
issue also resulted in a Division II EDG failure during a subsequent surveillance test.
Discussion
:  On October 18, 2004, a blown fuse in the electrical circuit that supplies 125 VDC power to the Division II EDG DC oil pumps starter resulted in the failure of the
pumps to operate. The Division II diesel generator was declared inoperable.
17 In Apparent Cause Evaluation (ACE) 267857, the licensee determined that the apparent cause of the F5-1 fuse failure was due to a high current overload combined with
potential fatigue of the fuse. However, the ACE also concluded that discoloration in the
F5 fuse holder could not be characterized as a high resistance point. The high current
condition was determined to be caused by high inrush current. The ACE stated that the
manufacturer does not recommend this fuse type for significant inrush current.
Corrective actions included an evaluation to change the fuse type and an evaluation to
do thermography on the fuse block during subsequent performance of CPS 3506.01.
The evaluation concluded that no change of fuse was necessary and thermography was
not viable. No other actions were recommended to determine the cause of the fuse
failure. On November 14, 2005, the Division II EDG DC oil pumps again failed to start during performance of CPS 3506.01 due to a failure of the 125 VDC circuit. This circuitry also
powered the fuel priming pump and the field conditioning relay. During the investigation
the licensee determined that the failure of the circuit was caused by a high resistance
electrical connection within the F5 and F5-1 fuse block.
Exelon PowerLabs report, CPS 83658 "Failure analysis of an ITE Gould, #FP32, 30A fuse block" concluded that dust and dirt accumulation internal to the fuse block stab
connection area in combination with accumulated, dried grease-like material that
provided a collection point for the dust and dirt caused the fuse block to fail. The
PowerLabs report could not determine whether the grease-like material was from the
fuse block manufacturer or not. The fuse block was original plant equipment. The
PowerLabs report indicated that it was evident based on the amount of dust and dirt
accumulated on the fuse block cover, that the environment in which the fuse was
installed was very dusty, and there were a number of passages on the fuse block that
would allow dust to accumulate.
An Apparent Cause Evaluation (ACE 398451) completed by the licensee stated that based on the results of the 2005 event and the PowerLabs report results, it was clear
that the degraded internal fuse block connection existed in 2004 and most probably was
the initiator of the 2004 event as well. Based on this information, the inspectors


concluded that the high resistance condition remained in the diesel circuitry for over a
=====Introduction:=====
The inspectors identified a Green finding involving a non-cited violation for inadequate corrective action. The licensees failure to properly identify and correct a degraded electrical circuit in 2004, resulted in the Division II EDG subsystem being vulnerable to electrical circuit failure if called upon to complete its support function. This issue also resulted in a Division II EDG failure during a subsequent surveillance test.


year despite there being signs that it existed following the first failure.
Discussion: On October 18, 2004, a blown fuse in the electrical circuit that supplies 125 VDC power to the Division II EDG DC oil pumps starter resulted in the failure of the pumps to operate. The Division II diesel generator was declared inoperable.


The inspectors concluded that failure of Apparent Cause Evaluation 264857 to properly identify the cause of high resistance in the fuse connection resulted in a repetitive failure
In Apparent Cause Evaluation (ACE) 267857, the licensee determined that the apparent cause of the F5-1 fuse failure was due to a high current overload combined with potential fatigue of the fuse. However, the ACE also concluded that discoloration in the F5 fuse holder could not be characterized as a high resistance point. The high current condition was determined to be caused by high inrush current. The ACE stated that the manufacturer does not recommend this fuse type for significant inrush current.


of the Division II 125V DC oil pumps (turbo soak back and circulating pumps) auto-start
Corrective actions included an evaluation to change the fuse type and an evaluation to do thermography on the fuse block during subsequent performance of CPS 3506.01.


feature during the performance of CPS 3506.01.
The evaluation concluded that no change of fuse was necessary and thermography was not viable. No other actions were recommended to determine the cause of the fuse failure.


Following a review of the PowerLabs report and ACE 398451, the inspectors were concerned with the licensee's extent of condition review and subsequent corrective
On November 14, 2005, the Division II EDG DC oil pumps again failed to start during performance of CPS 3506.01 due to a failure of the 125 VDC circuit. This circuitry also powered the fuel priming pump and the field conditioning relay. During the investigation the licensee determined that the failure of the circuit was caused by a high resistance electrical connection within the F5 and F5-1 fuse block.


actions related to this issue. The inspectors noted that the ACE contained no
Exelon PowerLabs report, CPS 83658 Failure analysis of an ITE Gould, #FP32, 30A fuse block concluded that dust and dirt accumulation internal to the fuse block stab connection area in combination with accumulated, dried grease-like material that provided a collection point for the dust and dirt caused the fuse block to fail. The PowerLabs report could not determine whether the grease-like material was from the fuse block manufacturer or not. The fuse block was original plant equipment. The PowerLabs report indicated that it was evident based on the amount of dust and dirt accumulated on the fuse block cover, that the environment in which the fuse was installed was very dusty, and there were a number of passages on the fuse block that would allow dust to accumulate.


information that addressed why this particular fuse and fuse holder was unique or had a
An Apparent Cause Evaluation (ACE 398451) completed by the licensee stated that based on the results of the 2005 event and the PowerLabs report results, it was clear that the degraded internal fuse block connection existed in 2004 and most probably was the initiator of the 2004 event as well. Based on this information, the inspectors concluded that the high resistance condition remained in the diesel circuitry for over a year despite there being signs that it existed following the first failure.


higher susceptibility of being found in this degraded condition (dried grease and dirt on
The inspectors concluded that failure of Apparent Cause Evaluation 264857 to properly identify the cause of high resistance in the fuse connection resulted in a repetitive failure of the Division II 125V DC oil pumps (turbo soak back and circulating pumps) auto-start feature during the performance of CPS 3506.01.


contacts). As a result of questions by the inspectors related to extent of condition and
Following a review of the PowerLabs report and ACE 398451, the inspectors were concerned with the licensees extent of condition review and subsequent corrective actions related to this issue. The inspectors noted that the ACE contained no information that addressed why this particular fuse and fuse holder was unique or had a higher susceptibility of being found in this degraded condition (dried grease and dirt on contacts). As a result of questions by the inspectors related to extent of condition and subsequent corrective actions, the licensee developed actions to examine other fuse and fuse holders in the Divisions I and III 125 VDC electrical circuitry in an expedited manner.
 
subsequent corrective actions, the licensee developed actions to examine other fuse 18 and fuse holders in the Divisions I and III 125 VDC electrical circuitry in an expedited manner.  


=====Analysis:=====
=====Analysis:=====
Failure to correctly identify the cause of the 2004 Division II EDG 125 VDC circuit failure was a performance deficiency. The inspectors determined that the finding
Failure to correctly identify the cause of the 2004 Division II EDG 125 VDC circuit failure was a performance deficiency. The inspectors determined that the finding was greater than minor in accordance with IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue Disposition Screening, issued September 30, 2005. This issue was greater than minor because the finding affected the Mitigating Systems Cornerstone objective of ensuring the availability, reliability, and capability of mitigating systems to prevent undesirable consequences. The inspectors evaluated this finding using Manual Chapter 0609, Significance Determination Process, Appendix A, Significance Determination of Reactor Inspection Findings for At-Power Situations, Phase 1 screening associated with the Mitigating Systems Cornerstone. The 125 VDC system is a backup to the AC oil system in case of a loss of offsite power. Offsite power was not lost, therefore, there was not an actual loss of safety function for the diesel.
 
was greater than minor in accordance with IMC 0612, "Power Reactor Inspection
 
Reports," Appendix B, "Issue Disposition Screening," issued September 30, 2005. This
 
issue was greater than minor because the finding affected the Mitigating Systems
 
Cornerstone objective of ensuring the availability, reliability, and capability of mitigating
 
systems to prevent undesirable consequences. The inspectors evaluated this finding
 
using Manual Chapter 0609, "Significance Determination Process," Appendix A, "Significance Determination of Reactor Inspection Findings for At-Power Situations,"
 
Phase 1 screening associated with the Mitigating Systems Cornerstone. The 125 VDC
 
system is a backup to the AC oil system in case of a loss of offsite power. Offsite power was not lost, therefore, there was not an actual loss of safety function for the diesel.


This was a Green issue.
This was a Green issue.


=====Enforcement:=====
=====Enforcement:=====
10 CFR 50, Appendix B, Criterion XVI, states that measures shall be established to assure that conditions adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and equipment, and non-conformances are
10 CFR 50, Appendix B, Criterion XVI, states that measures shall be established to assure that conditions adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and equipment, and non-conformances are promptly identified and corrected. Contrary to the above, following a failure of the Division II EDG 125 VDC circuit on November 14, 2004, the licensee failed to identify and correct the deficiency that caused the failure. This was a violation. Corrective actions by the licensee included replacing the fuse and fuse holder and expediting actions to address the extent of condition relative to the as-found condition of the fuse and fuse holder.
 
promptly identified and corrected. Contrary to the above, following a failure of the
 
Division II EDG 125 VDC circuit on November 14, 2004, the licensee failed to identify
 
and correct the deficiency that caused the failure. This was a violation. Corrective
 
actions by the licensee included replacing the fuse and fuse holder and expediting


actions to address the extent of condition relative to the as-found condition of the fuse
The finding also affected the cross-cutting area of problem identification and resolution since the licensee failed to adequately address the degraded circuit condition in a timely manner. Because the finding has been captured by the licensees corrective action program (CR 398451), this violation is being treated as a non-cited violation (NCV 05000461/2005-09-02(DRP)) consistent with Section VI.A.1 of the NRC Enforcement Policy.
 
and fuse holder.
 
The finding also affected the cross-cutting area of problem identification and resolution since the licensee failed to adequately address the degraded circuit condition in a timely
 
manner. Because the finding has been captured by the licensee's corrective action
 
program (CR 398451), this violation is being treated as a non-cited violation (NCV 05000461/2005-09-02(DRP))
consistent with Section VI.A.1 of the NRC Enforcement Policy.
{{a|1R23}}
{{a|1R23}}
==1R23 Temporary Plant Modifications (71111.23)==
==1R23 Temporary Plant Modifications==
{{IP sample|IP=IP 71111.23}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed temporary plant modifications to verify that the instructions were consistent with applicable design modification documents and that the
The inspectors reviewed temporary plant modifications to verify that the instructions were consistent with applicable design modification documents and that the modifications did not adversely impact system operability or availability. The inspectors interviewed operations, engineering and maintenance personnel as appropriate and reviewed the design modification documents and the 10 CFR 50.59 evaluations against the applicable portions of the USAR. The documents listed at the end of this report were also used by the inspectors to evaluate this area.
 
modifications did not adversely impact system operability or availability. The inspectors interviewed operations, engineering and maintenance personnel as appropriate and
 
reviewed the design modification documents and the 10 CFR 50.59 evaluations against
 
the applicable portions of the USAR. The documents listed at the end of this report were
 
also used by the inspectors to evaluate this area.
 
The inspectors reviewed the issues that the licensee entered into its corrective action program to verify that identified temporary modification problems were being entered into
 
the program with the appropriate characterization and significance. The inspectors also 19 reviewed the licensee's corrective actions for temporary modification related issues documented in selected condition reports. The condition reports are specified in the list
 
of documents reviewed. The inspectors completed two inspection samples by reviewing


the following temporary modifications:*Install temporary power supply as a backup to power supply Item 69 in panel 1PA05J*Division III emergency diesel generator high water temperature switch
The inspectors reviewed the issues that the licensee entered into its corrective action program to verify that identified temporary modification problems were being entered into the program with the appropriate characterization and significance. The inspectors also reviewed the licensees corrective actions for temporary modification related issues documented in selected condition reports. The condition reports are specified in the list of documents reviewed. The inspectors completed two inspection samples by reviewing the following temporary modifications:
* Install temporary power supply as a backup to power supply Item 69 in panel 1PA05J
* Division III emergency diesel generator high water temperature switch


====b. Findings====
====b. Findings====
No findings of significance were identified.1EP4Emergency Action Level and Emergency Plan Changes (71114.04)
No findings of significance were identified.
{{a|1EP4}}
==1EP4 Emergency Action Level and Emergency Plan Changes==
{{IP sample|IP=IP 71114.04}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors performed a screening review of Revision 7 of the Clinton Power Station Annex to the Exelon Standardized Emergency Plan to determine whether the changes
The inspectors performed a screening review of Revision 7 of the Clinton Power Station Annex to the Exelon Standardized Emergency Plan to determine whether the changes made in Revision 7 decreased the effectiveness of the licensees emergency planning.


made in Revision 7 decreased the effectiveness of the licensee's emergency planning.
The screening review of this revision did not constitute an approval of the changes and, as such, the changes are subject to future NRC inspection to ensure that the emergency plan continues to meet NRC regulations.
 
The screening review of this revision did not constitute an approval of the changes and, as such, the changes are subject to future NRC inspection to ensure that the emergency
 
plan continues to meet NRC regulations.


These activities completed one inspection sample.
These activities completed one inspection sample.


====b. Findings====
====b. Findings====
No findings of significance were identified.1EP6Drill Evaluation (71114.06)
No findings of significance were identified.
{{a|1EP6}}
==1EP6 Drill Evaluation==
{{IP sample|IP=IP 71114.06}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors observed the emergency response activities associated with drills and focused training conducted on December 12, and 15, 2005. Specifically, the inspectors
The inspectors observed the emergency response activities associated with drills and focused training conducted on December 12, and 15, 2005. Specifically, the inspectors verified that the emergency classification and simulated notifications were properly completed, and that the licensee adequately critiqued the training. Additionally, the inspectors observed licensee activities during the site accountability drill in the designated assembly area at the Operational Support Center (OSC) to ensure the drill was conducted in accordance with licensee procedures. The inspectors reviewed issue reports generated as a result of the drill and discussed these discrepancies with the site emergency preparedness manager. The inspectors completed two inspection samples by observing these emergency preparedness evolutions:
 
* Site accountability drill
verified that the emergency classification and simulated notifications were properly
* Table-top drill scenarios CPS PI #s 3 & 4
 
completed, and that the licensee adequately critiqued the training. Additionally, the
 
inspectors observed licensee activities during the site accountability drill in the
 
designated assembly area at the Operational Support Center (OSC) to ensure the drill
 
was conducted in accordance with licensee procedures. The inspectors reviewed issue
 
reports generated as a result of the drill and discussed these discrepancies with the site
 
emergency preparedness manager. The inspectors completed two inspection samples
 
by observing these emergency preparedness evolutions:*Site accountability drill*Table-top drill scenarios CPS PI #'s 3 & 4


====b. Findings====
====b. Findings====
20 No findings of significance were identified.2.
No findings of significance were identified.


==RADIATION SAFETY==
==RADIATION SAFETY==
2OS1Access Control To Radiologically Significant Areas (71121.01).1Review of Licensee Performance Indicators for the Occupational Exposure Cornerstone
2OS1 Access Control To Radiologically Significant Areas (71121.01)
 
===.1 Review of Licensee Performance Indicators for the Occupational Exposure Cornerstone===


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the licensee's occupational exposure control cornerstone Performance Indicators (PIs) to determine whether or not the conditions surrounding the
The inspectors reviewed the licensees occupational exposure control cornerstone Performance Indicators (PIs) to determine whether or not the conditions surrounding the PIs had been evaluated, and identified problems had been entered into the corrective action program for resolution. This review represented one sample.
 
PIs had been evaluated, and identified problems had been entered into the corrective
 
action program for resolution. This review represented one sample.


====b. Findings====
====b. Findings====
Line 944: Line 447:


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed procedures and methods for controlling airborne radioactivity areas to evaluate barrier integrity and engineering controls performance (e.g., high
The inspectors reviewed procedures and methods for controlling airborne radioactivity areas to evaluate barrier integrity and engineering controls performance (e.g., high efficiency particulate air (HEPA) ventilation system operation) and to determine if there was a potential for individual worker internal exposures of greater than 50 millirem committed effective dose equivalent. There were no airborne areas created as a result of major activities observed during the inspection. This review represented one sample.


efficiency particulate air (HEPA) ventilation system operation) and to determine if there
The adequacy of the licensees internal dose assessment process for internal exposures greater than 50 millirem committed effective dose equivalent was assessed. There were no internal exposures greater than 50 millirem. This review represented one sample.


was a potential for individual worker internal exposures of greater than 50 millirem
====b. Findings====
No findings of significance were identified.


committed effective dose equivalent. There were no airborne areas created as a result
===.3 Problem Identification and Resolution===
 
of major activities observed during the inspection. This review represented one sample.
 
The adequacy of the licensee's internal dose assessment process for internal exposures greater than 50 millirem committed effective dose equivalent was assessed. There were
 
no internal exposures greater than 50 millirem. This review represented one sample.
 
====b. Findings====
No findings of significance were identified..3Problem Identification and Resolution


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the licensee's self-assessments, audits, licensee event reports, and special reports related to the access control program to determine if identified
The inspectors reviewed the licensees self-assessments, audits, licensee event reports, and special reports related to the access control program to determine if identified problems were entered into the corrective action program for resolution. This review represented one sample.


problems were entered into the corrective action program for resolution. This review
The inspectors reviewed corrective action reports related to access controls and high radiation area radiological incidents (non-performance indicators identified by the licensee in high radiation areas less than 1R/hr). Staff members were interviewed and corrective action documents were reviewed to determine if follow-up activities were being conducted in an effective and timely manner commensurate with their importance to safety and risk based on the following:
* Initial problem identification, characterization, and tracking
* Disposition of operability/reportability issues
* Evaluation of safety significance/risk and priority for resolution
* Identification of repetitive problems
* Identification of contributing causes
* Identification and implementation of effective corrective actions
* Resolution of non-cited violations (NCVs) tracked in the corrective action system
* Implementation/consideration of risk significant operational experience feedback This review represented one sample.


represented one sample.
The inspectors evaluated the licensees process for problem identification, characterization, and prioritization and determined if problems were entered into the corrective action program and resolved. For repetitive deficiencies and/or significant individual deficiencies in problem identification and resolution, the inspectors determined if the licensees self-assessment activities were capable of identifying and addressing these deficiencies. This review represented one sample.


The inspectors reviewed corrective action reports related to access controls and high radiation area radiological incidents (non-performance indicators identified by the 21 licensee in high radiation areas less than 1R/hr). Staff members were interviewed and corrective action documents were reviewed to determine if follow-up activities were
The inspectors reviewed licensee documentation packages for all PI events occurring since the last inspection to determine if any of these PI events involved dose rates greater than 25 R/hr at 30 centimeters or greater than 500 R/hr at 1 meter. Barriers were evaluated for failure and to determine if there were any barriers left to prevent personnel access. There were no PI events occurring since the last inspection. This review represented one sample.


being conducted in an effective and timely manner commensurate with their importance
====b. Findings====
 
No findings of significance were identified.
to safety and risk based on the following:*Initial problem identification, characterization, and tracking*Disposition of operability/reportability issues
*Evaluation of safety significance/risk and priority for resolution
*Identification of repetitive problems
*Identification of contributing causes
*Identification and implementation of effective corrective actions
*Resolution of non-cited violations (NCVs) tracked in the corrective action system
*Implementation/consideration of risk significant operational experience feedback This review represented one sample.
 
The inspectors evaluated the licensee's process for problem identification, characterization, and prioritization and determined if problems were entered into the


corrective action program and resolved. For repetitive deficiencies and/or significant individual deficiencies in problem identification and resolution, the inspectors determined
===.4 Job-In-Progress Reviews===
 
if the licensee's self-assessment activities were capable of identifying and addressing
 
these deficiencies. This review represented one sample.
 
The inspectors reviewed licensee documentation packages for all PI events occurring since the last inspection to determine if any of these PI events involved dose rates
 
greater than 25 R/hr at 30 centimeters or greater than 500 R/hr at 1 meter. Barriers
 
were evaluated for failure and to determine if there were any barriers left to prevent
 
personnel access. There were no PI events occurring since the last inspection. This
 
review represented one sample.
 
====b. Findings====
No findings of significance were identified..4Job-In-Progress Reviews


====a. Inspection Scope====
====a. Inspection Scope====
Radiological work in high radiation work areas having significant dose rate gradients was reviewed to evaluate the application of dosim etry to effectively monitor exposure to personnel and to verify that licensee controls were adequate. These work areas
Radiological work in high radiation work areas having significant dose rate gradients was reviewed to evaluate the application of dosimetry to effectively monitor exposure to personnel and to verify that licensee controls were adequate. These work areas involved areas where the dose rate gradients were severe which increased the necessity of providing multiple dosimeters and/or enhanced job controls. This review represented one sample.
 
involved areas where the dose rate gradients were severe which increased the necessity
 
of providing multiple dosimeters and/or enhanced job controls. This review represented
 
one sample.


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified.


22.5High Risk Significant, High Dose Rate and Very High Radiation Area Controls
===.5 High Risk Significant, High Dose Rate and Very High Radiation Area Controls===


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors held discussions with the radiation protection manager concerning high dose rate/high radiation area and very high radiation area controls and procedures, including procedural changes that had occurred since the last inspection, in order to
The inspectors held discussions with the radiation protection manager concerning high dose rate/high radiation area and very high radiation area controls and procedures, including procedural changes that had occurred since the last inspection, in order to determine if any procedure modifications did not substantially reduce the effectiveness and level of worker protection. This review represented one sample.


determine if any procedure modifications did not substantially reduce the effectiveness
The inspectors discussed with Radiation Protection (RP) supervisors the controls that were in place for special areas that had the potential to become very high radiation areas during certain plant operations, to determine if these plant operations required communication beforehand with the RP group, so as to allow corresponding timely actions to properly post and control the radiation hazards. This review represented one sample.


and level of worker protection. This review represented one sample.
The inspectors conducted plant walkdowns to evaluate the posting and locking of entrances to high dose rate and very high radiation areas. This review represented one sample.


The inspectors discussed with Radiation Protection (RP) supervisors the controls that were in place for special areas that had the potential to become very high radiation
====b. Findings====
No findings of significance were identified.


areas during certain plant operations, to determine if these plant operations required
2OS2 As Low As Is Reasonably Achievable Planning And Controls (ALARA) (71121.02)


communication beforehand with the RP group, so as to allow corresponding timely
===.1 Problem Identification and Resolutions===
 
actions to properly post and control the radiation hazards. This review represented one sample.The inspectors conducted plant walkdowns to evaluate the posting and locking of entrances to high dose rate and very high radiation areas. This review represented one sample.
 
====b. Findings====
No findings of significance were identified.2OS2As Low As Is Reasonably Achievable Planning And Controls (ALARA) (71121.02).1Problem Identification and Resolutions


====a. Inspection Scope====
====a. Inspection Scope====
The licensee's corrective action program was reviewed to determine if repetitive deficiencies in problem identification and resolution were being addressed. This review
The licensees corrective action program was reviewed to determine if repetitive deficiencies in problem identification and resolution were being addressed. This review represented one sample.
 
represented one sample.


====b. Findings====
====b. Findings====
Line 1,045: Line 510:
==4OA1 Performance Indicator Verification==
==4OA1 Performance Indicator Verification==
{{IP sample|IP=IP 71151}}
{{IP sample|IP=IP 71151}}
.1Radiation Safety Strategic Area
===.1 Radiation Safety Strategic Area===


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the licensee draft data collections used to prepare submittals for two PIs. The inspectors used PI guidance and definitions contained in Nuclear 23 Energy Institute (NEI) Document 99-02, Revision 3, "Regulatory Assessment Performance Indicator Guideline," to evaluate the accuracy of the PI data. As part of the
The inspectors reviewed the licensee draft data collections used to prepare submittals for two PIs. The inspectors used PI guidance and definitions contained in Nuclear Energy Institute (NEI) Document 99-02, Revision 3, Regulatory Assessment Performance Indicator Guideline, to evaluate the accuracy of the PI data. As part of the inspection, the documents listed in Appendix 1 were utilized to evaluate the accuracy of PI data. The inspectors' review included, but was not limited to, conditions and data from logs, licensee event reports, condition reports, and calculations for each PI specified.
 
inspection, the documents listed in Appendix 1 were utilized to evaluate the accuracy of
 
PI data. The inspectors' review included, but was not limited to, conditions and data
 
from logs, licensee event reports, condition reports, and calculations for each PI
 
specified.


The following PIs were reviewed:
The following PIs were reviewed:
*Occupational Exposure Control Effectiveness, for the period of January 2005 through October 2005*RETS/ODCM Radiological Effluent Occurrence, for the period of September 2004 through July 2005
* Occupational Exposure Control Effectiveness, for the period of January 2005 through October 2005
* RETS/ODCM Radiological Effluent Occurrence, for the period of September 2004 through July 2005


====b. Findings====
====b. Findings====
Line 1,069: Line 527:


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the Clinton Power Station initial license training root cause analysis for poor performance on the NRC initial license examination conducted in
The inspectors reviewed the Clinton Power Station initial license training root cause analysis for poor performance on the NRC initial license examination conducted in July 2005 for correct identification of the causes of initial license training applicant performance. The inspectors compared applicant experience/background with initial license training program admission requirements. The inspectors reviewed the training program used to prepare the applicants for the initial operator license examination. The inspectors reviewed applicant written examination/quiz grades and performance reviews associated with their simulator control room integrated plant operations training. The inspectors reviewed the results of performance review committees and performance review boards for compliance with station procedures and initial license training program academic requirements. The inspectors interviewed several station operations instructors, licensed operators, operations management, and training management to determine their understanding of program requirements, initial license training candidate progress, and the initial license training lead instructor contribution to the program. The inspectors reviewed the recommended corrective actions contained within the root cause analysis for adequacy and accuracy.
 
July 2005 for correct identification of the causes of initial license training applicant
 
performance. The inspectors compared applicant experience/background with initial
 
license training program admission requirements. The inspectors reviewed the training
 
program used to prepare the applicants for the initial operator license examination. The
 
inspectors reviewed applicant written examination/quiz grades and performance reviews
 
associated with their simulator control room integrated plant operations training. The
 
inspectors reviewed the results of performance review committees and performance
 
review boards for compliance with station procedures and initial license training program
 
academic requirements. The inspectors interviewed several station operations
 
instructors, licensed operators, operations management, and training management to
 
determine their understanding of program requirements, initial license training candidate
 
progress, and the initial license training lead instructor contribution to the program. The
 
inspectors reviewed the recommended corrective actions contained within the root
 
cause analysis for adequacy and accuracy.


====b. Findings====
====b. Findings====
Discussion
Discussion: The inspectors determined that the root cause analysis was thorough and identified the causes of poor performance by the initial operator license applicants. The inspectors determined that the applicants met all entrance requirements into the license class without exception. One clarification was received from Region III to ensure one applicant met all license requirements. The training program had been successfully used to train previous license classes and the initial license training lead instructor was attempting to emulate previous successful license classes by implementing the same schedule and program previously used. The inspectors determined that station management had failed to adequately support an inexperienced initial license training lead trainer during a critical portion of the license class training program. During that time the stations training director and operations training manager were not present at the site to provide oversight for the initial license training program. The initial license training lead trainer had to make several critical decisions without the guidance of an experienced manager, and lacking experience, made decisions that resulted in a class inadequately prepared to take the NRCs initial license examination. The initial license training lead trainers decisions resulted in remediation training not being completed in a timely manner with a resultant inadequate knowledge base upon which the applicants could build additional knowledge. Because of the lack of management supervision and initial license training lead trainer inexperience, inadequate documentation was provided to performance review boards to have applicants removed from the initial license training program. The inspectors noted that comments concerning the operational relevance of some of the written examination questions during the stations internal review were dismissed without adequate follow-up on the part of the examination author and others on the examination security agreement. The inspectors determined that the root cause analysis had discovered the failure causes for the poor performance and made accurate recommendations for corrective actions to prevent recurrence of the poor performance issues. The inspectors determined that if the recommended corrective actions are fully implemented and maintained, a recurrence of the poor performance will be avoided.
: The inspectors determined that the root cause analysis was thorough and identified the causes of poor performance by the initial operator license applicants. The
 
inspectors determined that the applicants met all entrance requirements into the license
 
class without exception. One clarification was received from Region III to ensure one
 
applicant met all license requirements. The training program had been successfully 24 used to train previous license classes and the initial license training lead instructor was attempting to emulate previous successful license classes by implementing the same
 
schedule and program previously used. The inspectors determined that station
 
management had failed to adequately support an inexperienced initial license training
 
lead trainer during a critical portion of the license class training program. During that
 
time the station's training director and operation's training manager were not present at
 
the site to provide oversight for the initial license training program. The initial license
 
training lead trainer had to make several critical decisions without the guidance of an
 
experienced manager, and lacking experience, made decisions that resulted in a class
 
inadequately prepared to take the NRC's initial license examination. The initial license
 
training lead trainer's decisions resulted in remediation training not being completed in a
 
timely manner with a resultant inadequate knowledge base upon which the applicants
 
could build additional knowledge. Because of the lack of management supervision and
 
initial license training lead trainer inexperience, inadequate documentation was provided
 
to performance review boards to have applicants removed from the initial license training
 
program. The inspectors noted that comments concerning the operational relevance of
 
some of the written examination questions during the station's internal review were
 
dismissed without adequate follow-up on the part of the examination author and others
 
on the examination security agreement. The inspectors determined that the root cause
 
analysis had discovered the failure causes for the poor performance and made accurate
 
recommendations for corrective actions to prevent recurrence of the poor performance
 
issues. The inspectors determined that if the recommended corrective actions are fully
 
implemented and maintained, a recurrence of the poor performance will be avoided.


===.2 Review and Assessment of Issue Report for Trends, Rigor, and Common-Cause===
===.2 Review and Assessment of Issue Report for Trends, Rigor, and Common-Cause===
Line 1,156: Line 537:


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors noted a slight increase in the number of plant issues involving equipment reliability. Some of these issues resulted in issue reports (IR) being generated by the
The inspectors noted a slight increase in the number of plant issues involving equipment reliability. Some of these issues resulted in issue reports (IR) being generated by the licensee. The inspectors reviewed issue reports with a focus on instrument out-of-tolerance IR with approved evaluations from January 2004 through November 2005.
 
licensee. The inspectors reviewed issue reports with a focus on instrument
 
out-of-tolerance IR with approved evaluations from January 2004 through
 
November 2005.


====b. Findings====
====b. Findings====
No findings of significance were identified. However, the inspectors noted that the licensee failed to follow and meet the intent of the instrument trending program as
No findings of significance were identified. However, the inspectors noted that the licensee failed to follow and meet the intent of the instrument trending program as described in licensee administrative procedure ER-AA-520 Instrument Trending Program. Specifically, the licensee engineering staff failed to meet the management and program expectations to have the trending report and engineering analysis completed 60 days after completion of a refueling outage. This expectation promotes a timely review and evaluation of instrumentation issues such as suitability for application.
 
described in licensee administrative procedure ER-AA-520 "Instrument Trending
 
Program.Specifically, the licensee engi neering staff failed to meet the management and program expectations to have the trending report and engineering analysis


completed 60 days after completion of a refueling outage. This expectation promotes a
Timely evaluations would allow for adequate planning and work scheduling for replacement of unreliable instrumentation.


timely review and evaluation of instrumentation issues such as suitability for application.
Specifically, Section 4.4 of ER-AA-520, instrument performance trending, stated that once per operating cycle, engineering would run a trend report on the condition report database. The procedure required system managers to review the report and evaluate instruments associated with their systems. Evaluations for what should be considered an adverse trend would be included in this report. This procedure also required that site design engineering evaluate the trend report for indication of common mode failures once per operating cycle and perform a drift analysis for those instruments in the As-Found/As-Left program. The procedure directed site design engineering to update the drift analysis for the make/model groups. Any issues identified related to common mode failures or instrumentation issues that would affect the drift analysis required corrective actions be created to correct the issue. As stated in ER-AA-520, this procedure provided the administrative process for the instrument trending program and it also provided control of the As-Found/As-left analysis program. This program maintained the analysis conducted as part of the 24-month cycle extension project as required by Generic Letter 91-04.


Timely evaluations would allow for adequate planning and work scheduling for
The licensee adopted ER-AA-520 in 2002 during Cycle 9. On November 16, 2005, inspectors requested a copy of the instrument trending program analysis completed in accordance with ER-AA-520. The licensee had not completed a finalized trend report or instrument analysis as directed by ER-AA-520. When questioned by the inspectors on why this report had not been completed, the licensee stated that the instrument trend report analysis was not completed due to poor program ownership by design engineering management.


replacement of unreliable instrumentation.
The inspectors review of the corrective action system did not identify any evidence of an actual loss of safety function of any mitigating system due to an out-of-tolerance instrumentation issue. The ninth refueling cycle ended February 2004, and the tenth refueling cycle will end on January 30, 2006. Therefore, the licensee has until that time to be in compliance with the procedural requirement.


Specifically, Section 4.4 of ER-AA-520, "instrument performance trending," stated that once per operating cycle, engineering would run a trend report on the condition report 25 database. The procedure required system managers to review the report and evaluate instruments associated with their systems. Evaluations for what should be considered
{{a|4OA6}}
==4OA6 Meetings==


an adverse trend would be included in this report. This procedure also required that site
===.1 Exit Meeting===


design engineering evaluate the trend report for indication of common mode failures
The inspectors presented the inspection results to Mr. Robert Bement and other members of licensee management at the conclusion of the inspection on January 12, 2005. The inspectors asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.


once per operating cycle and perform a drift analysis for those instruments in the
===.2 Interim Exit Meetings===


As-Found/As-Left program. The procedure directed site design engineering to update
Interim exits were conducted for:
* Emergency Preparedness inspection with Mr. M. Friedman on December 1, 2005
* Biennial Operator Requalification Program Inspection with Mr. R. Bement, Clinton Power Station Site Vice President, on November 23, 2005.


the drift analysis for the make/model groups. Any issues identified related to common
ATTACHMENT:  
 
mode failures or instrumentation issues that would affect the drift analysis required
 
corrective actions be created to correct the issue. As stated in ER-AA-520, this
 
procedure provided the administrative proce ss for the instrument trending program and it also provided control of the As-Found/As-left analysis program. This program
 
maintained the analysis conducted as part of the 24-month cycle extension project as
 
required by Generic Letter 91-04.
 
The licensee adopted ER-AA-520 in 2002 during Cycle 9. On November 16, 2005, inspectors requested a copy of the instrument trending program analysis completed in
 
accordance with ER-AA-520. The licensee had not completed a finalized trend report or
 
instrument analysis as directed by ER-AA-520. When questioned by the inspectors on
 
why this report had not been completed, the licensee stated that the instrument trend
 
report analysis was not completed due to poor program ownership by design
 
engineering management.
 
The inspectors' review of the corrective acti on system did not identify any evidence of an actual loss of safety function of any mitigating system due to an out-of-tolerance
 
instrumentation issue. The ninth refueling cycle ended February 2004, and the tenth
 
refueling cycle will end on January 30, 2006. Therefore, the licensee has until that time
 
to be in compliance with the procedural requirement.4OA6Meetings.1Exit Meeting The inspectors presented the inspection results to Mr. Robert Bement and other members of licensee management at the conclusion of the inspection on
 
January 12, 2005. The inspectors asked the licensee whether any materials examined
 
during the inspection should be considered proprietary. No proprietary information was
 
identified..2Interim Exit Meetings Interim exits were conducted for:
*Emergency Preparedness inspection with Mr. M. Friedman on December 1, 2005
*Biennial Operator Requalification Program Inspection with Mr. R. Bement, Clinton Power Station Site Vice President, on November 23, 2005.
 
ATTACHMENT:


=SUPPLEMENTAL INFORMATION=
=SUPPLEMENTAL INFORMATION=
Line 1,260: Line 594:


===Opened===
===Opened===
05000461/2005009-01NCVFailure to provide adequate maintenance and work
: 05000461/2005009-01            NCV        Failure to provide adequate maintenance and work instruction is a performance deficiency
instruction is a performance deficiency05000461/2005009-02NCVFailure to correctly identify and correct the cause of
: 05000461/2005009-02            NCV        Failure to correctly identify and correct the cause of the 2005 125 VDC circuit failure was a performance deficiency
the 2005 125 VDC circuit failure was a performance
 
===Closed===
: 05000461/2005009-01            NCV        Failure to provide adequate maintenance and work instruction is a performance deficiency
: 05000461/2005009-02            NCV        Failure to correctly identify and correct the cause of the 2005 125 VDC circuit failure was a performance deficiency


deficiency
===Discussed===


===Closed===
NONE
05000461/2005009-01NCVFailure to provide adequate maintenance and work
instruction is a performance deficiency05000461/2005009-02NCVFailure to correctly identify and correct the cause of
the 2005 125 VDC circuit failure was a performance


deficiency
Discussed NONE
==LIST OF DOCUMENTS REVIEWED==
==LIST OF DOCUMENTS REVIEWED==


}}
}}

Revision as of 22:47, 23 November 2019

IR 05000461-05-009, on 10/01-12/31/2005, Amergen Energy Company LLC, Clinton Power Station, Post Maintenance Testing and Surveillance Testing
ML060310367
Person / Time
Site: Clinton Constellation icon.png
Issue date: 01/30/2006
From: Ring M
NRC/RGN-III/DRP/RPB1
To: Crane C
Exelon Generation Co, Exelon Nuclear
References
IR-05-009
Download: ML060310367 (37)


Text

ary 30, 2006

SUBJECT:

CLINTON POWER STATION NRC INTEGRATED INSPECTION REPORT 05000461/2005009

Dear Mr. Crane:

On December 31, 2005, the US Nuclear Regulatory Commission (NRC) completed an integrated inspection at your Clinton Power Station. The enclosed report documents the inspection findings which were discussed on January 12, 2006, with Mr. R. Bement and other members of your staff.

This inspection examined activities conducted under your license as they relate to safety and to compliance with the Commissions rules and regulations and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

Based on the results of this inspection, the inspectors identified two findings of very low safety significance (Green). Both of these findings involved violations of NRC requirements.

However, because these violations were of very low safety significance and because the issues have been entered into the licensees corrective action program, the NRC is treating these issues as non-cited violations, in accordance with Section VI.A.1 of the NRCs Enforcement Policy.

If you contest the subject or severity of a non-cited violation, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, US Nuclear Regulatory Commission - Region III, 2443 Warrenville Road, Lisle, IL 60532-4352; the Director, Office of Enforcement, US Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector Office at the Clinton Power Station Facility. In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Mark A. Ring, Chief Branch 1 Division of Reactor Projects Docket No. 50-461 License No. NPF-62 Enclosure: Inspection Report No. 05000461/2005009 w/Attachment: Supplemental Information cc w/encl: Site Vice President - Clinton Power Station Plant Manager - Clinton Power Station Regulatory Assurance Manager - Clinton Power Station Chief Operating Officer Senior Vice President - Nuclear Services Vice President - Operations Support Vice President - Licensing and Regulatory Affairs Manager Licensing - Clinton Power Station Senior Counsel, Nuclear, Mid-West Regional Operating Group Document Control Desk - Licensing

SUMMARY OF FINDINGS

IR 05000461/2005009; AmerGen Energy Company LLC; 10/01/2005 - 12/31/2005; Clinton

Power Station; Post Maintenance Testing and Surveillance Testing.

This report covers a 3-month period of baseline resident inspection and announced baseline inspections on radiation protection, emergency preparedness and licensed operator requalification. The inspection was conducted by Region III inspectors and the resident inspectors. Two Green findings involving two non-cited violations (NCVs) were identified. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.

A. Inspector-Identified and Self Revealing Findings

Cornerstone: Mitigating Systems

Green.

A self-revealing finding involving a non-cited violation (NCV) of Technical Specification 5.4.1 Procedures, was identified. On September 30, 2005, the Division III emergency diesel generator failed to properly run following maintenance activities, due to the inadequate maintenance instructions. The inadequate maintenance instructions resulted in air being trapped in the governor oil system during the replacement of the governor's servo booster motor. The licensee determined that this issue was the result of a maintenance planners failure to follow administrative guidelines for technical review during the development of the maintenance instructions.

This issue resulted in extended outage and unavailability time for the emergency diesel generator.

The inspectors determined that despite the fact that the issue involved work in progress, this issue was more than minor because the finding affected the Mitigating Systems Cornerstone objective of ensuring the availability of mitigating systems to prevent undesirable consequences. The issue resulted in the emergency diesel generator being unavailable for longer than expected by the plant staff. Following the initial maintenance run of the diesel generator, operators declared that the diesel generator was available for use if needed to respond to an event. Corrective actions by the licensee included developing lesson-learned information to share with other maintenance planners. Additionally, the licensee planned to add technical guidance related to venting air from the diesel governor to the diesel maintenance training material. The finding also affected the cross cutting area of human performance since the licensees maintenance personnel failed to request technical guidance from the site engineering staff as directed by the licensees administrative procedures.

(Section 1R19)

Green.

The inspectors identified a finding involving a non-cited violation for inadequate corrective action. The licensees failure to properly identify and correct a degraded electrical circuit in 2004, involving a high resistance connection on a fuse holder, resulted in the Division II emergency diesel generator subsystem being vulnerable to electrical circuit failure if called upon to complete its support function. The high resistance connection was caused by degraded grease-like material and dirt. This issue also resulted in the Division II diesel generator failure during a subsequent surveillance test.

The inspectors determined that the finding was greater than minor because the finding affected the Mitigating Systems Cornerstone objective of ensuring the availability, reliability, and capability of mitigating systems to prevent undesirable consequences.

The Division II emergency diesel generator 125 VDC system is a backup to the AC oil system in case of a loss of offsite power. Offsite power was not lost, therefore, there was not an actual loss of safety function for the diesel. Corrective actions by the licensee included replacing the fuse and fuse holder and expediting actions to address the extent of condition relative to the as-found condition of the fuse and fuse holder. The finding also affected the cross cutting area of problem identification and resolution since the licensee failed to adequately address the degraded circuit condition in a timely manner. (Section 1R22)

Licensee-Identified Violations

No findings of significance were identified.

REPORT DETAILS

Summary of Plant Status

The plant operated at approximately 95.5 percent rated thermal power (maintaining 103 percent electrical output) throughout most of the inspection period. On November 18, 2005, reactor power was reduced to 85 percent to reseat a potentially stuck open moisture separator reheater relief valve. On November 19, 2005, plant operators returned reactor power to 95.5 percent.

On December 2, 2005, operators lowered reactor power to 49 percent in response to a ruptured main condenser tube and returned power to 95.5 percent on December 4, 2005. On December 18, 2005, operators lowered reactor power to 90 percent for a planned rod pattern adjustment (All rods out). Power was restored to 95 percent on December 18, 2005, and maintained there through the end of the inspection period.

REACTOR SAFETY

Cornerstone: Initiating Events, Mitigating Systems, Barrier Integrity, and Emergency

Preparedness

1R01 Adverse Weather

a. Inspection Scope

The inspectors reviewed the licensees seasonal readiness preparation checklist for cold weather and to verify that it adequately covered risk-significant equipment and ensured that the equipment was in a condition to meet the requirements of Technical Specifications (TS), the Operations Requirements Manual (ORM), and the Updated Safety Analysis Report (USAR) with respect to protection from low temperatures. The inspectors verified that minor issues identified during the inspection were entered into the licensees corrective action system by reviewing the associated Condition Reports (CR). The inspectors conducted more detailed system reviews and walkdowns for the reactor core isolation cooling storage tank and service air compressor intake. The inspectors also reviewed several issue reports related to main condenser tube leaks that seem to occur more frequently at the onset of cold weather. These issue reports and other documents reviewed during the inspection are listed at the end of this report. This activity represents one inspection sample.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignments

.1 Complete Semi-Annual

a. Inspection Scope

The inspectors conducted a complete system alignment inspection of the low pressure core spray (LPCS) system. This system was selected based on its high risk significance and mitigating systems function. The inspectors reviewed plant procedures, drawings, and the USAR to identify proper system alignment and visually inspected system valves, instrumentation, and electrical supplies to verify proper alignment, component accessibility, availability, and current material condition. The inspectors also completed a review of corrective action documents, work orders, and operator work around and challenges to ensure there were no current operability concerns with the system.

Documents reviewed during this inspection are listed in the Attachment. These activities completed one inspection sample.

b. Findings

No findings of significance were identified.

.2 Partial Walkdowns

a. Inspection Scope

The inspectors performed partial walkdowns of accessible portions of divisions of risk-significant mitigating systems equipment during times when the divisions were of increased importance due to the redundant divisions or other related equipment being unavailable. The inspectors utilized the valve and electric breaker checklists listed in the to verify that the components were properly positioned and that support systems were lined up as needed. The inspectors also examined the material condition of the components and observed operating parameters of equipment to verify that there were no obvious deficiencies. The inspectors reviewed outstanding work orders and CR associated with the divisions to verify that those documents did not reveal issues that could affect division function. The inspectors used the information in the appropriate sections of the USAR to determine the functional requirements of the systems. The documents listed at the end of this report were also used by the inspectors to evaluate this area. The inspectors performed two samples by verifying the alignment of the following divisions:

  • Auxiliary power system

b. Findings

No findings of significance were identified.

1R05 Fire Protection

a. Inspection Scope

The inspectors conducted fire protection walkdowns which were focused on availability, accessibility, and the condition of fire fighting equipment, the control of transient combustibles and ignition sources, and on the condition and operating status of installed fire barriers. The inspectors selected fire areas for inspection based on their overall contribution to internal fire risk, as documented in the individual plant examination of external events with later additional insights, their potential to impact equipment which could cause a plant transient, or their impact on the licensees ability to respond to a security event. The inspectors used the documents listed at the end of this report to verify that fire hoses and extinguishers were in their designated locations and available for immediate use, that fire detectors and sprinklers were not obstructed, that transient material loading was within the analyzed limits, and that fire doors, dampers, and penetration seals appeared to be in satisfactory condition. The inspectors verified that minor issues identified during the inspection were entered into the licensees corrective action program.

The inspectors reviewed portions of the licensees fire protection evaluation report and the USAR to verify consistency in the documented analysis with installed fire protection equipment at the station.

The inspectors completed four samples by inspection of the following areas:

C Fire zone A - 1a: Elevation 707' 6", General Access Area (North)

C Fire zone A - 2a: Elevation 707' 6", RCIC Pump Room C Fire zone A - 6: Elevation 707' 6", General Access Area (South)

C Fire zone CB-6a: Elevation 800' Main Control Room Complex

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program

.1 Facility Operating History

a. Inspection Scope

The inspectors reviewed the plants operating history from January 2004 through October 2005 to assess whether the licensed operator requalification training program had identified and addressed operator performance deficiencies at the plant.

b. Findings

No findings of significance were identified.

.2 Licensee Requalification Examinations

a. Inspection Scope

The inspectors performed a biennial inspection of the licensees licensed operator requalification training test/examination program. The operating examination material reviewed consisted of four operating tests, each containing approximately two dynamic simulator scenarios and approximately five job performance measures. The written examinations reviewed consisted of four written examinations, each containing approximately 35 questions. The inspectors reviewed the annual requalification operating test and biennial written examination material to evaluate general quality, construction, and difficulty level. The inspectors assessed the level of examination material duplication from week-to-week during the current year operating test, and compared the operating test material from this years operating tests (2005) with last years operating tests (2004). The annual operating tests were conducted in September/October/November 2004 and September/October/November 2005. The examiners assessed the amount of written examination material duplication from week-to-week for the written examination administered in September/October/November 2005. The inspectors reviewed the methodology for developing the examinations, including the licensed operator requalification training program two year sample plan, probabilistic risk assessment insights, previously identified operator performance deficiencies, and plant modifications.

b. Findings

No findings of significance were identified.

.3 Licensee Administration of Requalification Examinations

a. Inspection Scope

The inspectors observed the administration of a requalification operating test to assess the licensees effectiveness in conducting the test. The inspectors evaluated the performance of one shift crew in parallel with the facility evaluators during two dynamic simulator scenarios and evaluated various licensed crew members concurrently with facility evaluators during the administration of several job performance measures. The inspectors assessed the facility evaluators ability to determine adequate crew and individual performance using objective, measurable standards. The inspectors observed the training staff personnel administer the operating test, including conducting pre-examination briefings, evaluations of operator performance, and individual and crew evaluations upon completion of the operating test. The inspectors evaluated the ability of the simulator to support the examinations. A specific evaluation of simulator performance was conducted and documented under Section 1R11.9, Conformance With Simulator Requirements Specified in 10 CFR 55.46, of this report.

b. Findings

No findings of significance were identified.

.4 Examination Security

a. Inspection Scope

The inspectors observed and reviewed the licensees overall licensed operator requalification examination security program related to examination physical security (e.g., access restrictions and simulator considerations) and integrity (e.g., predictability and bias). The inspectors also reviewed the facility licensees examination security procedure, any corrective actions related to past or present examination security problems at the facility, and the implementation of security and integrity measures (e.g., security agreements, sampling criteria, bank use, and test item repetition)throughout the examination process.

b. Findings

No findings of significance were identified.

.5 Licensee Training Feedback System

a. Inspection Scope

The inspectors assessed the methods and effectiveness of the licensees processes for revising and maintaining its licensed operator requalification training program up to date, including the use of feedback from plant events and industry experience information.

The inspectors reviewed the licensees quality assurance oversight activities, including licensee training department self-assessment reports. The inspectors evaluated the licensees ability to assess the effectiveness of its licensed operator requalification training program and the licensees ability to implement appropriate corrective actions.

b. Findings

No findings of significance were identified.

.6 Licensee Remedial Training Program

a. Inspection Scope

The inspectors assessed the adequacy and effectiveness of the remedial training conducted since the previous biennial requalification examinations and the training planned for the current examination cycle to ensure that the licensee addressed weaknesses in licensed operator or crew performance identified during training and plant operations. The inspectors reviewed remedial training procedures and individual remedial training plans.

b. Findings

No findings of significance were identified.

.7 Conformance With Operator License Conditions

a. Inspection Scope

The inspectors reviewed the facility and individual operator licensees' conformance with the requirements of 10 CFR Part 55. The inspectors reviewed the facility licensee's program for maintaining active operator licenses and to assess compliance with 10 CFR 55.53

(e) and (f). The inspectors reviewed the procedural guidance and the process for tracking on-shift hours for licensed operators and which control room positions were granted watch-standing credit for maintaining active operator licenses.

The inspectors reviewed the facility licensee's licensed operator requalification training program to assess compliance with the requalification program requirements as described by 10 CFR 55.59 (c). Additionally, medical records for 16 licensed operators were reviewed for compliance with 10 CFR 55.53 (i).

b. Findings

No findings of significance were identified.

.8 Annual Operating Test Results

a. Inspection Scope

The inspector reviewed the overall pass/fail results of the annual operating examination which consisted of job performance measure and simulator operating tests (required per 10 CFR 55.59(a)(2)) administered by the licensee. The inspectors reviewed the overall pass/fail results for the biennial written examination (required per 10 CFR 55.59(a)(2))

administered by the licensee. The overall results were compared with the significance determination process in accordance with NRC Manual Chapter 0609I, Operator Requalification Human Performance Significance Determination Process (SDP). This represented one sample.

b. Findings

No findings of significance were identified.

.9 Conformance With Simulator Requirements Specified in 10 CFR 55.46

a. Inspection Scope

The inspectors assessed the adequacy of the licensees simulation facility (simulator) for use in operator licensing examinations and for satisfying experience requirements as prescribed in 10 CFR 55.46, Simulation Facilities. The inspectors also reviewed a sample of simulator performance test records (i.e., transient tests, scenario test and discrepancy resolution validation test), simulator discrepancy and modification records, and the process for ensuring continued assurance of simulator fidelity in accordance with 10 CFR 55.46. The inspectors reviewed and evaluated the discrepancy process to ensure that simulator fidelity was maintained. Open simulator discrepancies were reviewed for importance relative to the impact on 10 CFR 55.45 and 55.59 operator actions as well as on nuclear and thermal hydraulic operating characteristics. The inspectors conducted interviews with members of the licensees simulator staff about the configuration control process and completed the IP 71111.11, Appendix C, checklist to evaluate whether or not the licensees plant-referenced simulator was operating adequately as required by 10 CFR 55.46

(c) and (d).

b. Findings

No findings of significance were identified.

.10 Quarterly Resident Inspector Review

a. Inspection Scope

The inspectors reviewed licensed-operator requalification training to evaluate operator performance in mitigating the consequences of a simulated event, particularly in the areas of human performance. The inspectors evaluated operator performance attributes which included communication clarity and formality, timely performance of appropriate operator actions, appropriate alarm response, proper procedure use and adherence, and senior reactor operator oversight and command and control.

Crew performance in these areas was compared to licensee management expectations and guidelines as presented in the following documents:

  • ESG-LOR-85 - Loss of 6.9 kV Bus 1B, ATWS - Drywell Leak
  • ESG-LOR-74 - Steam Leak, Drywell Leak, Figure N Blowdown
  • OP-AA-101-111, Roles and Responsibilities of On-shift Personnel, Rev 0
  • OP-AA-106-101, Significant Event Reporting, Rev 2 The inspectors also assessed the performance of the training staff evaluators involved in the requalification process. For any weaknesses identified, the inspectors observed that the licensee evaluators also noted the issues and discussed them in the critique at the end of the session. The inspectors verified all issues were captured in the training program and licensee corrective action process.

These activities completed two inspection samples.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness

The inspectors reviewed the effectiveness of the licensees maintenance efforts in implementing the Maintenance Rule (MR) requirements, including a review of scoping, goal-setting, performance monitoring, short and long-term corrective actions, and current equipment performance problems. Systems were selected based on their designation as risk significant under the maintenance rule, or being in the increased monitoring (MR category (a) (1)) group. In addition, the inspectors interviewed the system engineers and maintenance rule coordinator. The inspectors also reviewed condition reports and associated documents for appropriate identification of problems, entry into the corrective action system, and appropriateness of planned or completed actions. The documents reviewed are listed at the end of the report. The inspectors completed two samples by reviewing the following:

  • Containment ventilation system and continuous containment purge system

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessment

The inspectors observed the licensees risk assessment processes and considerations used to plan and schedule maintenance activities on safety-related structures, systems, and components, particularly to ensure that maintenance risk and emergent work contingencies had been identified and resolved. The inspectors completed five samples by assessing the effectiveness of risk management activities for the following work activities or work weeks:

  • Emergency reserve auxiliary transformer system outage
  • Division I diesel generator ventilation fan control in pull-to-lock to support troubleshooting activities concurrent with planned maintenance on division 1 essential switchgear heat removal (WR# 189992)
  • Cumulative review of licensee risk management assessments following transfer of 1B1 Bus to the reserve auxiliary transformer and then back to the emergency reserve auxiliary transformer for post maintenance test on 1AP09EC synch check relay as directed by WO# 758834-02, division II standby gas treatment system out of service for planned maintenance, and division II essential switchgear heat removal fan and chiller out of service for planned maintenance
  • Licensee risk assessment activities and redundant system protection activities following a trip of the division III diesel during a monthly run

b. Findings

No findings of significance were identified.

1R14 Non-routine Evolutions

a. Inspection Scope

The inspectors reviewed personnel performance during planned and unplanned plant evolutions and selected licensee event reports focusing on those involving personnel response to non-routine conditions. The review was performed to ascertain that operator responses were in accordance with the required procedures. In particular, the inspectors completed one sample by reviewing personnel performance during the following plant event:

  • Plant Operations activities in response to main condenser tube failure

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations

a. Inspection Scope

The inspectors reviewed the following operability determinations and evaluations affecting mitigating systems to determine whether operability was properly justified and the component or system remained available such that no unrecognized risk increase had occurred. The inspectors completed three samples of operability determinations and evaluations by reviewing the following:

  • Division II diesel generator - failure of division II DC oil pumps to keep running due to a high current overload on F5-1 fuse

b. Findings

No findings of significance were identified.

1R16 Operator Workarounds

.1 Review of selected workaround issue

a. Inspection Scope

The inspectors assessed the following operator workaround issue to determine the potential effects on the functionality of the corresponding system:

  • Condensate pump suction pressure - condensate pump suction pressure is degraded During this inspection, the inspectors reviewed the technical adequacy of the workaround documentation against the updated safety analysis report and other design information to assess whether the workaround conflicted with any design basis information. The inspectors compared the information in abnormal or emergency operating procedures to the workaround information to ensure that the operators maintained the ability to implement important procedures when needed.

This represented one inspection sample.

b. Findings

No findings of significance were identified.

.2 Semi-annual Review of the Cumulative Effects of Operator Workarounds

a. Inspection Scope

The inspectors reviewed all operator workarounds and challenges to identify any potential effect on mitigating systems ability to function as required during emergencies and ensure that operators would be able to respond in a correct and timely manner to plant transients and accidents. The inspectors utilized procedure OP-AA-102-103, Operator Work-Around Program, revision 1, during the review. The inspectors also reviewed issue reports and work orders related to corrective actions to remove the workarounds or compensatory actions.

The inspectors completed one sample by reviewing the following workarounds and challenges:

  • N66-D006B off gas regenerator dryer thermostatic trap
  • 1FW01 PB turbine-driven reactor feed pump 1B
  • 1WS026 turbine oil cooler temperature control valve
  • Condensate pump suction pressure
  • 0WE01FA (B) [C] radwaste filters A (B) [C]

b. Findings

No findings of significance were identified.

1R19 Post Maintenance Testing

a. Inspection Scope

The inspectors reviewed the post maintenance testing activities associated with maintenance or modification of important mitigating, barrier integrity, and support systems that were identified as risk significant in the licensees risk analysis. The inspectors reviewed these activities to verify that the post maintenance testing was performed adequately, demonstrated that the maintenance was successful, and that operability was restored. During this inspection activity, the inspectors interviewed maintenance and engineering department personnel and reviewed the completed post maintenance testing documentation. The inspectors used the appropriate sections of the TS and USAR, as well as the documents listed at the end of this report, to evaluate this area.

Testing subsequent to the following activities was observed and evaluated to complete seven inspection samples:

  • Reviewed completed CPS 3412.01, Essential switchgear heat removal, following completion of WO# 752802, 1SX202A relief valve and 1SX110BA pipe replacement
  • Standby Gas Treatment Train B - containment draw down test following work to correct flow oscillations WO# 657204, OP 9065.02 OP secondary containment integrity; January 18, 2004, and WO# 655681, IM Flow indication oscillating

+/- 400 scfm; November 22, 2005

  • Division III diesel generator high water temperature switch replacement
  • Reviewed Section 8.14.18 of CPS 9061.06C014 to ensure post maintenance testing adequacy following removal of deluge line flange and reinstallation of spool piece for 1SX073B standby gas treatment 1B deluge valve
  • Reviewed CPS 3412.01, Essential switchgear heat removal, following completion of WO #616616, circuit breaker and bucket replacement
  • Reviewed results of CPS 8731.12 following rod control and information system transponder card replacement WO# 647415

b. Findings

Introduction:

A self-revealing Green finding involving a non-cited violation (NCV) of Technical Specification 5.4 Procedures, was identified. On September 30, 2005, the Division III emergency diesel generator (EDG) failed to properly run following maintenance activities, due to inadequate maintenance instructions. The licensee determined that this issue was the result of a maintenance planners failure to follow administrative guidelines for technical review during the development of the maintenance instructions. This issue resulted in extended outage and unavailability time of the EDG.

Discussion: On September 30, 2005, the Division III EDG was started for a maintenance run following a system outage window. During the initial start of the EDG, the start sequence was normal. Followup adjustments were then made on a newly installed shutdown solenoid. The licensees operations staff declared the diesel generator available if needed to response to an event. The licensees online risk profile changed from Yellow to Green. At this time compensatory actions such as the establishment of protected system pathways were removed.

During subsequent starts, the EDG exhibited abnormal starting indication. While starting the EDG for post maintenance test, the licensee observed a starting time of greater than 12 seconds. Additionally, unusual speed and voltage variations occurred when operators made adjustments to the diesel voltage regulator while the diesel was running.

A licensee investigation determined that due to a lack of technical rigor for EDG shutdown solenoid and servo booster replacement, the work instructions performing these tasks contained inadequate guidance which allowed air to be trapped in the servo booster motor. The servo booster motor is a part of the governor. The air trapped on the oil side of the governors operating piston resulted in the governor not being able to perform its designed function. This issue resulted in lengthening the time in which the Division III EDG was unavailable and inoperable.

The licensees investigation also determined that the work instructions failed to contain adequate instructions for venting or draining air from the governor following the replacement of the servo booster. The licensee concluded that this issue would not have occurred if the work planner responsible for the work instructions would have contacted the appropriate engineering staff per the licensees Performance Centered Maintenance (MA-AA-716-210) procedure. This procedure required the maintenance planner to route the work instructions to the licensees engineering staff for a formal review of technical information.

Analysis:

Failure to provide adequate maintenance and work instruction is a performance deficiency. The inspectors compared this finding to the findings identified in Appendix E, Examples of Minor Issues, of IMC 0612, Power Reactor Inspection Reports, dated September 30, 2005, to determine whether the finding was minor. The inspectors determined that no example contained in Appendix E was applicable to this situation. The inspectors then reviewed this finding against the guidance contained in Appendix B, Issue Dispositioning Screening, of IMC 0612. The inspectors determined that despite the fact that this issue involved work in progress, this issue was more than minor because the finding affected the Mitigating Systems Cornerstone objective of ensuring the availability of mitigating systems to prevent undesirable consequences.

The issue resulted in the emergency diesel generator being unavailable for longer than expected by the plant staff. Following the initial maintenance run of the diesel generator operators declared that the diesel generator was available for use, if needed to respond to an event. At this time, a number of compensatory actions such as the establishment of protected system pathways were eliminated. The inspectors completed a Phase 1 significance determination of this issue using IMC 0609, Significance Determination Process, Appendix A, Attachment 1, dated November 22, 2005. The inspectors selected the Mitigating Systems Cornerstone. The inspectors answered no to all five questions. Therefore, the inspectors concluded that this issue was a finding of very low safety significance (Green).

Enforcement:

Technical Specification 5.4.1, states that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.

Appendix A of Regulatory Guide 1.33, recommends that procedures for performing maintenance that can affect the performance of safety-related equipment should be properly preplanned and performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances.

Contrary to the above, the licensees procedures for performing maintenance on the Division III EDG were inadequate, in that, the work instruction did not prevent air from being trapped in the servo booster motor and did not vent the air following the servo booster replacement. On September 30, 2005, the licensees failure to have adequate maintenance procedures resulted in the diesel generator not operating properly. This was a violation. Corrective actions by the licensee included developing lesson-learned information so issues surrounding this finding would be shared with other licensee staff.

Additionally, the licensee planned to add technical guidance related to venting air from the diesel governor to the licensees diesel maintenance training material.

The finding also affected the cross cutting area of human performance since the licensees maintenance personnel failed to request formal technical guidance from engineering staff as directed by licensee administrative procedures. Because the finding has been captured by the licensees corrective action program (CR 379980), this violation is being treated as a non-cited violation (NCV 05000461/200509-01(DRP))

consistent with Section VI.A.1 of the NRC Enforcement Policy.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors witnessed selected surveillance testing and/or reviewed test data to verify that the equipment tested using the surveillance procedures met the TS, the ORM, the USAR, and licensee procedural requirements, and demonstrated that the equipment was capable of performing its intended safety functions. The activities were selected based on their importance in verifying mitigating systems capability and barrier integrity.

The inspectors used the documents listed at the end of this report to verify that the testing met the frequency requirements; that the tests were conducted in accordance with the procedures, including establishing the proper plant conditions and prerequisites; that the test acceptance criteria were met; and that the results of the tests were properly reviewed and recorded. In addition, the inspectors interviewed operations, maintenance and engineering department personnel regarding the tests and test results.

The inspectors evaluated the following surveillance tests to complete six inspection samples:

  • CPS 9080.02 Diesel Generator 1B Operability - Manual Quick Start Operability
  • CPS 9080.03 Diesel Generator 1C Operability - Manual Quick Start Operability

b. Findings

Introduction:

The inspectors identified a Green finding involving a non-cited violation for inadequate corrective action. The licensees failure to properly identify and correct a degraded electrical circuit in 2004, resulted in the Division II EDG subsystem being vulnerable to electrical circuit failure if called upon to complete its support function. This issue also resulted in a Division II EDG failure during a subsequent surveillance test.

Discussion: On October 18, 2004, a blown fuse in the electrical circuit that supplies 125 VDC power to the Division II EDG DC oil pumps starter resulted in the failure of the pumps to operate. The Division II diesel generator was declared inoperable.

In Apparent Cause Evaluation (ACE) 267857, the licensee determined that the apparent cause of the F5-1 fuse failure was due to a high current overload combined with potential fatigue of the fuse. However, the ACE also concluded that discoloration in the F5 fuse holder could not be characterized as a high resistance point. The high current condition was determined to be caused by high inrush current. The ACE stated that the manufacturer does not recommend this fuse type for significant inrush current.

Corrective actions included an evaluation to change the fuse type and an evaluation to do thermography on the fuse block during subsequent performance of CPS 3506.01.

The evaluation concluded that no change of fuse was necessary and thermography was not viable. No other actions were recommended to determine the cause of the fuse failure.

On November 14, 2005, the Division II EDG DC oil pumps again failed to start during performance of CPS 3506.01 due to a failure of the 125 VDC circuit. This circuitry also powered the fuel priming pump and the field conditioning relay. During the investigation the licensee determined that the failure of the circuit was caused by a high resistance electrical connection within the F5 and F5-1 fuse block.

Exelon PowerLabs report, CPS 83658 Failure analysis of an ITE Gould, #FP32, 30A fuse block concluded that dust and dirt accumulation internal to the fuse block stab connection area in combination with accumulated, dried grease-like material that provided a collection point for the dust and dirt caused the fuse block to fail. The PowerLabs report could not determine whether the grease-like material was from the fuse block manufacturer or not. The fuse block was original plant equipment. The PowerLabs report indicated that it was evident based on the amount of dust and dirt accumulated on the fuse block cover, that the environment in which the fuse was installed was very dusty, and there were a number of passages on the fuse block that would allow dust to accumulate.

An Apparent Cause Evaluation (ACE 398451) completed by the licensee stated that based on the results of the 2005 event and the PowerLabs report results, it was clear that the degraded internal fuse block connection existed in 2004 and most probably was the initiator of the 2004 event as well. Based on this information, the inspectors concluded that the high resistance condition remained in the diesel circuitry for over a year despite there being signs that it existed following the first failure.

The inspectors concluded that failure of Apparent Cause Evaluation 264857 to properly identify the cause of high resistance in the fuse connection resulted in a repetitive failure of the Division II 125V DC oil pumps (turbo soak back and circulating pumps) auto-start feature during the performance of CPS 3506.01.

Following a review of the PowerLabs report and ACE 398451, the inspectors were concerned with the licensees extent of condition review and subsequent corrective actions related to this issue. The inspectors noted that the ACE contained no information that addressed why this particular fuse and fuse holder was unique or had a higher susceptibility of being found in this degraded condition (dried grease and dirt on contacts). As a result of questions by the inspectors related to extent of condition and subsequent corrective actions, the licensee developed actions to examine other fuse and fuse holders in the Divisions I and III 125 VDC electrical circuitry in an expedited manner.

Analysis:

Failure to correctly identify the cause of the 2004 Division II EDG 125 VDC circuit failure was a performance deficiency. The inspectors determined that the finding was greater than minor in accordance with IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue Disposition Screening, issued September 30, 2005. This issue was greater than minor because the finding affected the Mitigating Systems Cornerstone objective of ensuring the availability, reliability, and capability of mitigating systems to prevent undesirable consequences. The inspectors evaluated this finding using Manual Chapter 0609, Significance Determination Process, Appendix A, Significance Determination of Reactor Inspection Findings for At-Power Situations, Phase 1 screening associated with the Mitigating Systems Cornerstone. The 125 VDC system is a backup to the AC oil system in case of a loss of offsite power. Offsite power was not lost, therefore, there was not an actual loss of safety function for the diesel.

This was a Green issue.

Enforcement:

10 CFR 50, Appendix B, Criterion XVI, states that measures shall be established to assure that conditions adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and equipment, and non-conformances are promptly identified and corrected. Contrary to the above, following a failure of the Division II EDG 125 VDC circuit on November 14, 2004, the licensee failed to identify and correct the deficiency that caused the failure. This was a violation. Corrective actions by the licensee included replacing the fuse and fuse holder and expediting actions to address the extent of condition relative to the as-found condition of the fuse and fuse holder.

The finding also affected the cross-cutting area of problem identification and resolution since the licensee failed to adequately address the degraded circuit condition in a timely manner. Because the finding has been captured by the licensees corrective action program (CR 398451), this violation is being treated as a non-cited violation (NCV 05000461/2005-09-02(DRP)) consistent with Section VI.A.1 of the NRC Enforcement Policy.

1R23 Temporary Plant Modifications

a. Inspection Scope

The inspectors reviewed temporary plant modifications to verify that the instructions were consistent with applicable design modification documents and that the modifications did not adversely impact system operability or availability. The inspectors interviewed operations, engineering and maintenance personnel as appropriate and reviewed the design modification documents and the 10 CFR 50.59 evaluations against the applicable portions of the USAR. The documents listed at the end of this report were also used by the inspectors to evaluate this area.

The inspectors reviewed the issues that the licensee entered into its corrective action program to verify that identified temporary modification problems were being entered into the program with the appropriate characterization and significance. The inspectors also reviewed the licensees corrective actions for temporary modification related issues documented in selected condition reports. The condition reports are specified in the list of documents reviewed. The inspectors completed two inspection samples by reviewing the following temporary modifications:

  • Install temporary power supply as a backup to power supply Item 69 in panel 1PA05J

b. Findings

No findings of significance were identified.

1EP4 Emergency Action Level and Emergency Plan Changes

a. Inspection Scope

The inspectors performed a screening review of Revision 7 of the Clinton Power Station Annex to the Exelon Standardized Emergency Plan to determine whether the changes made in Revision 7 decreased the effectiveness of the licensees emergency planning.

The screening review of this revision did not constitute an approval of the changes and, as such, the changes are subject to future NRC inspection to ensure that the emergency plan continues to meet NRC regulations.

These activities completed one inspection sample.

b. Findings

No findings of significance were identified.

1EP6 Drill Evaluation

a. Inspection Scope

The inspectors observed the emergency response activities associated with drills and focused training conducted on December 12, and 15, 2005. Specifically, the inspectors verified that the emergency classification and simulated notifications were properly completed, and that the licensee adequately critiqued the training. Additionally, the inspectors observed licensee activities during the site accountability drill in the designated assembly area at the Operational Support Center (OSC) to ensure the drill was conducted in accordance with licensee procedures. The inspectors reviewed issue reports generated as a result of the drill and discussed these discrepancies with the site emergency preparedness manager. The inspectors completed two inspection samples by observing these emergency preparedness evolutions:

  • Site accountability drill
  • Table-top drill scenarios CPS PI #s 3 & 4

b. Findings

No findings of significance were identified.

RADIATION SAFETY

2OS1 Access Control To Radiologically Significant Areas (71121.01)

.1 Review of Licensee Performance Indicators for the Occupational Exposure Cornerstone

a. Inspection Scope

The inspectors reviewed the licensees occupational exposure control cornerstone Performance Indicators (PIs) to determine whether or not the conditions surrounding the PIs had been evaluated, and identified problems had been entered into the corrective action program for resolution. This review represented one sample.

b. Findings

No findings of significance were identified.

.2 Plant Walkdowns and Radiation Work Permit Reviews

a. Inspection Scope

The inspectors reviewed procedures and methods for controlling airborne radioactivity areas to evaluate barrier integrity and engineering controls performance (e.g., high efficiency particulate air (HEPA) ventilation system operation) and to determine if there was a potential for individual worker internal exposures of greater than 50 millirem committed effective dose equivalent. There were no airborne areas created as a result of major activities observed during the inspection. This review represented one sample.

The adequacy of the licensees internal dose assessment process for internal exposures greater than 50 millirem committed effective dose equivalent was assessed. There were no internal exposures greater than 50 millirem. This review represented one sample.

b. Findings

No findings of significance were identified.

.3 Problem Identification and Resolution

a. Inspection Scope

The inspectors reviewed the licensees self-assessments, audits, licensee event reports, and special reports related to the access control program to determine if identified problems were entered into the corrective action program for resolution. This review represented one sample.

The inspectors reviewed corrective action reports related to access controls and high radiation area radiological incidents (non-performance indicators identified by the licensee in high radiation areas less than 1R/hr). Staff members were interviewed and corrective action documents were reviewed to determine if follow-up activities were being conducted in an effective and timely manner commensurate with their importance to safety and risk based on the following:

  • Initial problem identification, characterization, and tracking
  • Disposition of operability/reportability issues
  • Evaluation of safety significance/risk and priority for resolution
  • Identification of repetitive problems
  • Identification of contributing causes
  • Identification and implementation of effective corrective actions
  • Resolution of non-cited violations (NCVs) tracked in the corrective action system
  • Implementation/consideration of risk significant operational experience feedback This review represented one sample.

The inspectors evaluated the licensees process for problem identification, characterization, and prioritization and determined if problems were entered into the corrective action program and resolved. For repetitive deficiencies and/or significant individual deficiencies in problem identification and resolution, the inspectors determined if the licensees self-assessment activities were capable of identifying and addressing these deficiencies. This review represented one sample.

The inspectors reviewed licensee documentation packages for all PI events occurring since the last inspection to determine if any of these PI events involved dose rates greater than 25 R/hr at 30 centimeters or greater than 500 R/hr at 1 meter. Barriers were evaluated for failure and to determine if there were any barriers left to prevent personnel access. There were no PI events occurring since the last inspection. This review represented one sample.

b. Findings

No findings of significance were identified.

.4 Job-In-Progress Reviews

a. Inspection Scope

Radiological work in high radiation work areas having significant dose rate gradients was reviewed to evaluate the application of dosimetry to effectively monitor exposure to personnel and to verify that licensee controls were adequate. These work areas involved areas where the dose rate gradients were severe which increased the necessity of providing multiple dosimeters and/or enhanced job controls. This review represented one sample.

b. Findings

No findings of significance were identified.

.5 High Risk Significant, High Dose Rate and Very High Radiation Area Controls

a. Inspection Scope

The inspectors held discussions with the radiation protection manager concerning high dose rate/high radiation area and very high radiation area controls and procedures, including procedural changes that had occurred since the last inspection, in order to determine if any procedure modifications did not substantially reduce the effectiveness and level of worker protection. This review represented one sample.

The inspectors discussed with Radiation Protection (RP) supervisors the controls that were in place for special areas that had the potential to become very high radiation areas during certain plant operations, to determine if these plant operations required communication beforehand with the RP group, so as to allow corresponding timely actions to properly post and control the radiation hazards. This review represented one sample.

The inspectors conducted plant walkdowns to evaluate the posting and locking of entrances to high dose rate and very high radiation areas. This review represented one sample.

b. Findings

No findings of significance were identified.

2OS2 As Low As Is Reasonably Achievable Planning And Controls (ALARA) (71121.02)

.1 Problem Identification and Resolutions

a. Inspection Scope

The licensees corrective action program was reviewed to determine if repetitive deficiencies in problem identification and resolution were being addressed. This review represented one sample.

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES (OA)

4OA1 Performance Indicator Verification

.1 Radiation Safety Strategic Area

a. Inspection Scope

The inspectors reviewed the licensee draft data collections used to prepare submittals for two PIs. The inspectors used PI guidance and definitions contained in Nuclear Energy Institute (NEI) Document 99-02, Revision 3, Regulatory Assessment Performance Indicator Guideline, to evaluate the accuracy of the PI data. As part of the inspection, the documents listed in Appendix 1 were utilized to evaluate the accuracy of PI data. The inspectors' review included, but was not limited to, conditions and data from logs, licensee event reports, condition reports, and calculations for each PI specified.

The following PIs were reviewed:

  • Occupational Exposure Control Effectiveness, for the period of January 2005 through October 2005
  • RETS/ODCM Radiological Effluent Occurrence, for the period of September 2004 through July 2005

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems

.1 Initial License Examination Root Cause

a. Inspection Scope

The inspectors reviewed the Clinton Power Station initial license training root cause analysis for poor performance on the NRC initial license examination conducted in July 2005 for correct identification of the causes of initial license training applicant performance. The inspectors compared applicant experience/background with initial license training program admission requirements. The inspectors reviewed the training program used to prepare the applicants for the initial operator license examination. The inspectors reviewed applicant written examination/quiz grades and performance reviews associated with their simulator control room integrated plant operations training. The inspectors reviewed the results of performance review committees and performance review boards for compliance with station procedures and initial license training program academic requirements. The inspectors interviewed several station operations instructors, licensed operators, operations management, and training management to determine their understanding of program requirements, initial license training candidate progress, and the initial license training lead instructor contribution to the program. The inspectors reviewed the recommended corrective actions contained within the root cause analysis for adequacy and accuracy.

b. Findings

Discussion: The inspectors determined that the root cause analysis was thorough and identified the causes of poor performance by the initial operator license applicants. The inspectors determined that the applicants met all entrance requirements into the license class without exception. One clarification was received from Region III to ensure one applicant met all license requirements. The training program had been successfully used to train previous license classes and the initial license training lead instructor was attempting to emulate previous successful license classes by implementing the same schedule and program previously used. The inspectors determined that station management had failed to adequately support an inexperienced initial license training lead trainer during a critical portion of the license class training program. During that time the stations training director and operations training manager were not present at the site to provide oversight for the initial license training program. The initial license training lead trainer had to make several critical decisions without the guidance of an experienced manager, and lacking experience, made decisions that resulted in a class inadequately prepared to take the NRCs initial license examination. The initial license training lead trainers decisions resulted in remediation training not being completed in a timely manner with a resultant inadequate knowledge base upon which the applicants could build additional knowledge. Because of the lack of management supervision and initial license training lead trainer inexperience, inadequate documentation was provided to performance review boards to have applicants removed from the initial license training program. The inspectors noted that comments concerning the operational relevance of some of the written examination questions during the stations internal review were dismissed without adequate follow-up on the part of the examination author and others on the examination security agreement. The inspectors determined that the root cause analysis had discovered the failure causes for the poor performance and made accurate recommendations for corrective actions to prevent recurrence of the poor performance issues. The inspectors determined that if the recommended corrective actions are fully implemented and maintained, a recurrence of the poor performance will be avoided.

.2 Review and Assessment of Issue Report for Trends, Rigor, and Common-Cause

Attributes

a. Inspection Scope

The inspectors noted a slight increase in the number of plant issues involving equipment reliability. Some of these issues resulted in issue reports (IR) being generated by the licensee. The inspectors reviewed issue reports with a focus on instrument out-of-tolerance IR with approved evaluations from January 2004 through November 2005.

b. Findings

No findings of significance were identified. However, the inspectors noted that the licensee failed to follow and meet the intent of the instrument trending program as described in licensee administrative procedure ER-AA-520 Instrument Trending Program. Specifically, the licensee engineering staff failed to meet the management and program expectations to have the trending report and engineering analysis completed 60 days after completion of a refueling outage. This expectation promotes a timely review and evaluation of instrumentation issues such as suitability for application.

Timely evaluations would allow for adequate planning and work scheduling for replacement of unreliable instrumentation.

Specifically, Section 4.4 of ER-AA-520, instrument performance trending, stated that once per operating cycle, engineering would run a trend report on the condition report database. The procedure required system managers to review the report and evaluate instruments associated with their systems. Evaluations for what should be considered an adverse trend would be included in this report. This procedure also required that site design engineering evaluate the trend report for indication of common mode failures once per operating cycle and perform a drift analysis for those instruments in the As-Found/As-Left program. The procedure directed site design engineering to update the drift analysis for the make/model groups. Any issues identified related to common mode failures or instrumentation issues that would affect the drift analysis required corrective actions be created to correct the issue. As stated in ER-AA-520, this procedure provided the administrative process for the instrument trending program and it also provided control of the As-Found/As-left analysis program. This program maintained the analysis conducted as part of the 24-month cycle extension project as required by Generic Letter 91-04.

The licensee adopted ER-AA-520 in 2002 during Cycle 9. On November 16, 2005, inspectors requested a copy of the instrument trending program analysis completed in accordance with ER-AA-520. The licensee had not completed a finalized trend report or instrument analysis as directed by ER-AA-520. When questioned by the inspectors on why this report had not been completed, the licensee stated that the instrument trend report analysis was not completed due to poor program ownership by design engineering management.

The inspectors review of the corrective action system did not identify any evidence of an actual loss of safety function of any mitigating system due to an out-of-tolerance instrumentation issue. The ninth refueling cycle ended February 2004, and the tenth refueling cycle will end on January 30, 2006. Therefore, the licensee has until that time to be in compliance with the procedural requirement.

4OA6 Meetings

.1 Exit Meeting

The inspectors presented the inspection results to Mr. Robert Bement and other members of licensee management at the conclusion of the inspection on January 12, 2005. The inspectors asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.

.2 Interim Exit Meetings

Interim exits were conducted for:

  • Biennial Operator Requalification Program Inspection with Mr. R. Bement, Clinton Power Station Site Vice President, on November 23, 2005.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee personnel

R. Bement, Site Vice President
M. McDowell, Plant Manager
J. Cunningham, Work Management Director
R. Davis, Radiation Protection Director
R. Frantz, Regulatory Assurance Representative
M. Friedman, Emergency Preparedness Manager
M. Hiter, Access Control Supervisor
W. Iliff, Regulatory Assurance Director
C. VanDenburgh, Nuclear Oversight Manager
J. Domitrovich, Maintenance Director
D. Schavey, Operations Director
J. Madden, Chemistry Manager
C. Williamson, Security Manager
R. Peak, Site Engineering Director
W. Carsky, Shift Operations Superintendent
M. Baetz, Licensed Operator Requalification Training Group Lead
J. Lindsey, Training Director
A. Bailey, Operations Training Manager

LIST OF ITEMS

OPENED, CLOSED AND DISCUSSED

Opened

05000461/2005009-01 NCV Failure to provide adequate maintenance and work instruction is a performance deficiency
05000461/2005009-02 NCV Failure to correctly identify and correct the cause of the 2005 125 VDC circuit failure was a performance deficiency

Closed

05000461/2005009-01 NCV Failure to provide adequate maintenance and work instruction is a performance deficiency
05000461/2005009-02 NCV Failure to correctly identify and correct the cause of the 2005 125 VDC circuit failure was a performance deficiency

Discussed

NONE

LIST OF DOCUMENTS REVIEWED