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{{#Wiki_filter:February 14, 2007Jeffrey S. Forbes, Vice President, Operations
{{#Wiki_filter:February 14, 2007
Arkansas Nuclear One  
Jeffrey S. Forbes, Vice President,
  Operations
Arkansas Nuclear One
Entergy Operations, Inc.
Entergy Operations, Inc.
1448 S.R. 333
1448 S.R. 333
Russellville, Arkansas 72801-0967SUBJECT:ARKANSAS NUCLEAR ONE - NRC INTEGRATED INSPECTION REPORT05000313/2006005 AND 05000368/2006005Dear Mr. Forbes:
Russellville, Arkansas 72801-0967
On December 31, 2006, the U.S. Nuclear Regulatory Commission (NRC) completed aninspection at your Arkansas Nuclear One, Units 1 and 2, facility. The enclosed integrated
SUBJECT: ARKANSAS NUCLEAR ONE - NRC INTEGRATED INSPECTION REPORT
            05000313/2006005 AND 05000368/2006005
Dear Mr. Forbes:
On December 31, 2006, the U.S. Nuclear Regulatory Commission (NRC) completed an
inspection at your Arkansas Nuclear One, Units 1 and 2, facility. The enclosed integrated
report documents the inspection findings, which were discussed on January 17, 2007, and
report documents the inspection findings, which were discussed on January 17, 2007, and
again on February 8, 2007, with you and other members of your staff.The inspection examined activities conducted under your licenses as they relate to safety andcompliance with the Commission's rules and regulations and with the conditions of your
again on February 8, 2007, with you and other members of your staff.
licenses. The inspectors reviewed selected procedures and records, observed activities, and
The inspection examined activities conducted under your licenses as they relate to safety and
interviewed personnel.The report documents five self-revealing findings of very low safety significance (Green). Threeof these findings were determined to involve violations of NRC requirements. However,
compliance with the Commission's rules and regulations and with the conditions of your
licenses. The inspectors reviewed selected procedures and records, observed activities, and
interviewed personnel.
The report documents five self-revealing findings of very low safety significance (Green). Three
of these findings were determined to involve violations of NRC requirements. However,
because of the very low safety significance and because they are entered into your corrective
because of the very low safety significance and because they are entered into your corrective
action program, the NRC is treating these findings as noncited violations consistent with
action program, the NRC is treating these findings as noncited violations consistent with
Section VI.A.1 of the NRC Enforcement Policy. If you contest these noncited violations, you
Section VI.A.1 of the NRC Enforcement Policy. If you contest these noncited violations, you
should provide a response within 30 days of the date of this inspection report, with the basis for
should provide a response within 30 days of the date of this inspection report, with the basis for
your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,
your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,
Line 36: Line 46:
76011-4005; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission,
76011-4005; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission,
Washington DC 20555-0001; and the NRC Resident Inspector at Arkansas Nuclear One,
Washington DC 20555-0001; and the NRC Resident Inspector at Arkansas Nuclear One,
Units 1 and 2, facility.In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, itsenclosure, and your response (if any) will be made available electronically for public inspection  
Units 1 and 2, facility.
Entergy Operations, Inc.-2-in the NRC Public Document Room or from the Publicly Available Records (PARS) componentof NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at
In accordance with 10 CFR 2.390 of the NRC's Rules of Practice, a copy of this letter, its
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).Sincerely, /RA/Jeffrey A. Clark, ChiefProject Branch E
enclosure, and your response (if any) will be made available electronically for public inspection
Division of Reactor ProjectsDockets:   50-313     50-368Licenses: DPR-51     NPF-6Enclosure:NRC Inspection Report 05000313/2006005 and 05000368/2006005
 
   w/Attachment: Supplemental Informationcc w/Enclosure:Senior Vice President  
Entergy Operations, Inc.                     -2-
in the NRC Public Document Room or from the Publicly Available Records (PARS) component
of NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
                                          Sincerely,
                                            /RA/
                                          Jeffrey A. Clark, Chief
                                          Project Branch E
                                          Division of Reactor Projects
Dockets: 50-313
          50-368
Licenses: DPR-51
          NPF-6
Enclosure:
NRC Inspection Report 05000313/2006005 and 05000368/2006005
   w/Attachment: Supplemental Information
cc w/Enclosure:
Senior Vice President
   & Chief Operating Officer
   & Chief Operating Officer
Entergy Operations, Inc.
Entergy Operations, Inc.
P.O. Box 31995
P.O. Box 31995
Jackson, MS 39286-1995Vice PresidentOperations Support
Jackson, MS 39286-1995
Vice President
Operations Support
Entergy Operations, Inc.
Entergy Operations, Inc.
P.O. Box 31995
P.O. Box 31995
Jackson, MS 39286-1995General Manager Plant OperationsEntergy Operations, Inc.
Jackson, MS 39286-1995
General Manager Plant Operations
Entergy Operations, Inc.
Arkansas Nuclear One
Arkansas Nuclear One
1448 S. R. 333
1448 S. R. 333
Russellville, AR 72802Director, Nuclear Safety AssuranceEntergy Operations, Inc.
Russellville, AR 72802
Arkansas Nuclear One  
Director, Nuclear Safety Assurance
Entergy Operations, Inc.
Arkansas Nuclear One
1448 S. R. 333
1448 S. R. 333
Russellville, AR 72802  
Russellville, AR 72802
Entergy Operations, Inc.-3-Manager, LicensingEntergy Operations, Inc.
 
Entergy Operations, Inc.               -3-
Manager, Licensing
Entergy Operations, Inc.
Arkansas Nuclear One
Arkansas Nuclear One
1448 S. R. 333
1448 S. R. 333
Russellville, AR 72802Director, Nuclear Safety & LicensingEntergy Operations, Inc.
Russellville, AR 72802
Director, Nuclear Safety & Licensing
Entergy Operations, Inc.
1340 Echelon Parkway
1340 Echelon Parkway
Jackson, MS 39213-8298Section Chief, Division of HealthRadiation Control Section
Jackson, MS 39213-8298
Arkansas Department of Health and  
Section Chief, Division of Health
  Human Services
Radiation Control Section
Arkansas Department of Health and
Human Services
4815 West Markham Street, Slot 30
4815 West Markham Street, Slot 30
Little Rock, AR 72205-3867Section Chief, Division of HealthEmergency Management Section
Little Rock, AR 72205-3867
Arkansas Department of Health and  
Section Chief, Division of Health
  Human Services
Emergency Management Section
Arkansas Department of Health and
Human Services
4815 West Markham Street, Slot 30
4815 West Markham Street, Slot 30
Little Rock, AR 72205-3867Manager, Washington Nuclear OperationsABB Combustion Engineering Nuclear
Little Rock, AR 72205-3867
  Power
Manager, Washington Nuclear Operations
ABB Combustion Engineering Nuclear
Power
12300 Twinbrook Parkway, Suite 330
12300 Twinbrook Parkway, Suite 330
Rockville, MD 20852County Judge of Pope CountyPope County Courthouse
Rockville, MD 20852
County Judge of Pope County
Pope County Courthouse
100 West Main Street
100 West Main Street
Russellville, AR 72801James Mallay Director, Regulatory Affairs
Russellville, AR 72801
James Mallay
Director, Regulatory Affairs
Framatome ANP
Framatome ANP
3815 Old Forest Road
3815 Old Forest Road
Lynchburg, VA 24501  
Lynchburg, VA 24501
Entergy Operations, Inc.-4-Electronic distribution by RIV:Regional Administrator (BSM1)DRP Director (ATH)DRS Director (DDC)DRS Deputy Director (RJC1)Senior Resident Inspector (RWD)Branch Chief, DRP/E (ZKD)Senior Project Engineer, DRP/E (VGG)Team Leader, DRP/TSS (RLN1)RITS Coordinator (MSH3)DRS STA (DAP)D. Cullison, OEDO RIV Coordinator (DGC)ROPreports
 
ANO Site Secretary (VLH)SUNSI Review Completed: _JAC__ADAMS:   Yes No   Initials: __JAC____   Publicly Available       
Entergy Operations, Inc.                     -4-
G   Non-Publicly Available    
Electronic distribution by RIV:
G   Sensitive   Non-SensitiveR:\_REACTORS\_ANO\2006\AN2006-05RP-RWD.wpdRIV:RI:DRP/ERI:DRP/ESRI:DRP/EC:DRS/OBCHYoungJEJoseyRWDeeseATGodyT-JACT-JACT-JAC/RA/2/5/20072/5/20072/5/20072/4/2007C:DRS/PSBC:DRS/EB1C:DRS/EB2C:DRP/EMPShannonWBJonesLJSmithJAClark/RA//RA//RA//RA/2/5/20072/1/20072/1/20072/14/2007OFFICIAL RECORD COPYT=Telephone           E=E-mail       F=Fax  
Regional Administrator (BSM1)
-1-EnclosureU.S. NUCLEAR REGULATORY COMMISSION REGION IVDockets:50-313, 50-368 Licenses:DPR-51, NPF-6
DRP Director (ATH)
Report:05000313/2006005 and 05000368/2006005
DRS Director (DDC)
Licensee:Entergy Operations, Inc.
DRS Deputy Director (RJC1)
Facility:Arkansas Nuclear One, Units 1 and 2
Senior Resident Inspector (RWD)
Location:Junction of Hwy. 64W and Hwy. 333 South Russellville, ArkansasDates:September 24 through December 31, 2006
Branch Chief, DRP/E (ZKD)
Inspectors:L. Carson II, Senior Health Physicist, Plant Support BranchR. Deese, Senior Resident Inspector
Senior Project Engineer, DRP/E (VGG)
J. Josey, Resident Inspector
Team Leader, DRP/TSS (RLN1)
J. Kirkland, Project Engineer
RITS Coordinator (MSH3)
R. Lantz, Senior Emergency Preparedness Inspector
DRS STA (DAP)
D. Livermore, Senior Project Engineer
D. Cullison, OEDO RIV Coordinator (DGC)
C. Paulk, Senior Reactor Inspector
ROPreports
C. Young, Resident InspectorAccompanyingPersonnel:S. Makor, Reactor InspectorApproved By:Jeffrey A. Clark, Chief, Project Branch EDivision of Reactor Projects  
ANO Site Secretary (VLH)
-2-EnclosureTABLE OF CONTENTSSUMMARY OF FINDINGS....................................................31R01Adverse Weather Protection.......................................61R02Evaluation of Changes, Tests, or Experiments .........................71R04Equipment Alignment.............................................71R05Fire Protection..................................................71R07Heat Sink Performance..........................................101R08Inservice Inspection Activities.....................................101R11Licensed Operator Requalification Program...........................131R12Maintenance Effectiveness.......................................131R13Maintenance Risk Assessments and Emergent Work Control.............141R15Operability Evaluations..........................................151R17Permanent Plant Modifications.....................................171R19Postmaintenance Testing........................................171R20Refueling and Outage Activities....................................181R22Surveillance Testing.............................................211EP4Emergency Action Level and Emergency Plan Changes.................221EP6Drill Evaluation.................................................22RADIATION SAFETY.......................................................232OS1Access Control To Radiologically Significant Areas.....................23OTHER ACTIVITIES........................................................244OA1PI Verification..................................................244OA2Identification and Resolution of Problems............................254OA3Followup of Events and Notices of Enforcement Discretion ..............284OA5  Other Activities.................................................294OA6Meetings, Including Exit..........................................31SUPPLEMENTAL INFORMATION............................................A-1KEY POINTS OF CONTACT................................................A-1LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED...........................A-1LIST OF DOCUMENTS REVIEWED..........................................A-2
SUNSI Review Completed: _JAC__ ADAMS: / Yes No Initials: __JAC____
LIST OF ACRONYMS......................................................A-9  
/ Publicly Available      G Non-Publicly Available   G Sensitive / Non-Sensitive
-3-EnclosureSUMMARY OF FINDINGSIR 05000313/2006005, 05000368/2006005; 09/24/2006 - 12/31/2006; Arkansas Nuclear One,Units 1 and 2; Fire Protection, Operability Evaluations, Refueling and Outage Activities, Follow-
R:\_REACTORS\_ANO\2006\AN2006-05RP-RWD.wpd
up of Events and Notices of Enforcement Discretion.This report covered a 3-month period of inspection by resident and regional specialistinspectors. Five Green findings, three of which were noncited violations were identified. The
RIV:RI:DRP/E              RI:DRP/E            SRI:DRP/E        C:DRS/OB
CHYoung                    JEJosey            RWDeese          ATGody
T-JAC                      T-JAC              T-JAC             /RA/
2/5/2007                  2/5/2007            2/5/2007          2/4/2007
C:DRS/PSB                C:DRS/EB1            C:DRS/EB2        C:DRP/E
MPShannon                WBJones              LJSmith          JAClark
        /RA/             /RA/                 /RA/             /RA/
2/5/2007                  2/1/2007            2/1/2007          2/14/2007
OFFICIAL RECORD COPY                                  T=Telephone   E=E-mail     F=Fax
 
              U.S. NUCLEAR REGULATORY COMMISSION
                                  REGION IV
Dockets:     50-313, 50-368
Licenses:   DPR-51, NPF-6
Report:     05000313/2006005 and 05000368/2006005
Licensee:   Entergy Operations, Inc.
Facility:   Arkansas Nuclear One, Units 1 and 2
Location:   Junction of Hwy. 64W and Hwy. 333 South
            Russellville, Arkansas
Dates:       September 24 through December 31, 2006
Inspectors: L. Carson II, Senior Health Physicist, Plant Support Branch
            R. Deese, Senior Resident Inspector
            J. Josey, Resident Inspector
            J. Kirkland, Project Engineer
            R. Lantz, Senior Emergency Preparedness Inspector
            D. Livermore, Senior Project Engineer
            C. Paulk, Senior Reactor Inspector
            C. Young, Resident Inspector
Accompanying
Personnel:   S. Makor, Reactor Inspector
Approved By: Jeffrey A. Clark, Chief, Project Branch E
            Division of Reactor Projects
                                      -1-                               Enclosure
 
                                      TABLE OF CONTENTS
SUMMARY OF FINDINGS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3
      1R01 Adverse Weather Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6
      1R02 Evaluation of Changes, Tests, or Experiments . . . . . . . . . . . . . . . . . . . . . . . . . 7
      1R04 Equipment Alignment . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7
      1R05 Fire Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7
      1R07 Heat Sink Performance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 10
      1R08 Inservice Inspection Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 10
      1R11 Licensed Operator Requalification Program . . . . . . . . . . . . . . . . . . . . . . . . . . . 13
      1R12 Maintenance Effectiveness . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 13
      1R13 Maintenance Risk Assessments and Emergent Work Control . . . . . . . . . . . . . 14
      1R15 Operability Evaluations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 15
      1R17 Permanent Plant Modifications . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17
      1R19 Postmaintenance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17
      1R20 Refueling and Outage Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 18
      1R22 Surveillance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 21
      1EP4 Emergency Action Level and Emergency Plan Changes . . . . . . . . . . . . . . . . . 22
      1EP6 Drill Evaluation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 22
RADIATION SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 23
      2OS1 Access Control To Radiologically Significant Areas . . . . . . . . . . . . . . . . . . . . . 23
OTHER ACTIVITIES . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 24
      4OA1 PI Verification . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .   24
      4OA2 Identification and Resolution of Problems . . . . . . . . . . . . . . . . . . . . . . . . . . . .                     25
      4OA3 Followup of Events and Notices of Enforcement Discretion . . . . . . . . . . . . . .                                 28
      4OA5 Other Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .   29
      4OA6 Meetings, Including Exit . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .         31
SUPPLEMENTAL INFORMATION . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .               A-1
KEY POINTS OF CONTACT . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .           A-1
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED . . . . . . . . . . . . . . . . . . . . . . . . . . .                             A-1
LIST OF DOCUMENTS REVIEWED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .                 A-2
LIST OF ACRONYMS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .   A-9
                                                        -2-                                                         Enclosure
 
                                      SUMMARY OF FINDINGS
IR 05000313/2006005, 05000368/2006005; 09/24/2006 - 12/31/2006; Arkansas Nuclear One,
Units 1 and 2; Fire Protection, Operability Evaluations, Refueling and Outage Activities, Follow-
up of Events and Notices of Enforcement Discretion.
This report covered a 3-month period of inspection by resident and regional specialist
inspectors. Five Green findings, three of which were noncited violations were identified. The
significance of most findings is indicated by their color (Green, White, Yellow, or Red) using
significance of most findings is indicated by their color (Green, White, Yellow, or Red) using
Inspection Manual Chapter 0609, "Significance Determination Process.Findings for which the
Inspection Manual Chapter 0609, Significance Determination Process. Findings for which the
significance determination process does not apply may be Green or be assigned a severity
significance determination process does not apply may be Green or be assigned a severity
level after NRC management's review. The NRC's program for overseeing the safe operation
level after NRC management's review. The NRCs program for overseeing the safe operation
of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight
of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight
Process," Revision 3, dated July 2000.A.NRC-Identified and Self-Revealing FindingsCornerstone: Initiating Events *Green. A self-revealing noncited violation of Unit 2 TechnicalSpecification 6.4.1.c, Fire Protection Program Implementation, was identified for
Process, Revision 3, dated July 2000.
the failure of maintenance personnel to follow Procedure EN-DC-127, "Control of
A.     NRC-Identified and Self-Revealing Findings
Hot Work and Ignition Sources," while performing hot work. Specifically, the
Cornerstone: Initiating Events
licensee failed to ensure that combustible material within 35 feet of the work area
        *       Green. A self-revealing noncited violation of Unit 2 Technical
was removed or protected. Consequently, torch cutting activities near the Unit 2
                Specification 6.4.1.c, Fire Protection Program Implementation, was identified for
containment sump strainer caused a nearby plastic bag containing used
                the failure of maintenance personnel to follow Procedure EN-DC-127, Control of
protective clothing to ignite. This issue was entered into the licensee's
                Hot Work and Ignition Sources, while performing hot work. Specifically, the
corrective action program as Condition Reports ANO-2-2006-1565 and Condition
                licensee failed to ensure that combustible material within 35 feet of the work area
Report ANO-2-2006-1701. A number of additional examples of hot work
                was removed or protected. Consequently, torch cutting activities near the Unit 2
activities that involved inadequate implementation of applicable hot work control
                containment sump strainer caused a nearby plastic bag containing used
procedures were also identified.The finding is greater than minor because it is associated with the protectionagainst external factors attribute of the initiating events cornerstone, and it
                protective clothing to ignite. This issue was entered into the licensee's
directly affects the cornerstone objective to limit the likelihood of those events
                corrective action program as Condition Reports ANO-2-2006-1565 and Condition
that upset plant stability and challenge critical safety functions during shutdown
                Report ANO-2-2006-1701. A number of additional examples of hot work
as well as power operations. Additionally, if left uncorrected, the practice of
                activities that involved inadequate implementation of applicable hot work control
conducting hot work in a manner that results in unintended combustion of nearby
                procedures were also identified.
materials would become a more significant safety concern in that it could result
                The finding is greater than minor because it is associated with the protection
in a fire in or near other risk important equipment. The finding is not suitable for
                against external factors attribute of the initiating events cornerstone, and it
evaluation with the significance determination process neither the fire protection
                directly affects the cornerstone objective to limit the likelihood of those events
significance determination process nor the shutdown operations significance
                that upset plant stability and challenge critical safety functions during shutdown
determination process address shutdown fire protection findings. However, the
                as well as power operations. Additionally, if left uncorrected, the practice of
finding is determined to be of very low safety significance by NRC management's
                conducting hot work in a manner that results in unintended combustion of nearby
review because the finding occurred while the unit was already in a cold
                materials would become a more significant safety concern in that it could result
shutdown condition, and the operability of equipment necessary to maintain safe  
                in a fire in or near other risk important equipment. The finding is not suitable for
-4-Enclosureshutdown was not challenged. The cause of the finding is related to thecrosscutting element of human performance associated with work practicesbecause the fire watch failed to use error prevention techniques like self
                evaluation with the significance determination process neither the fire protection
checking and peer checking which would have prevented the event
                significance determination process nor the shutdown operations significance
(Section 1R05).*Green. A self-revealing noncited violation of Unit 2 TechnicalSpecification 6.4.1.a, "Procedures," was identified when an operator failed to
                determination process address shutdown fire protection findings. However, the
close Valve 2DCH-11, resin sluice header drain valve, when securing from a
                finding is determined to be of very low safety significance by NRC managements
resin transfer as required by procedure. One week later, while aligning the plant
                review because the finding occurred while the unit was already in a cold
for alternate purification with Valve 2DCH-11 being out of position, an
                shutdown condition, and the operability of equipment necessary to maintain safe
unanticipated loss of approximately 230 gallons of reactor coolant system
                                                  -3-                                     Enclosure
inventory occurred. This issue was entered into the licensee's corrective action
 
program as Condition Report ANO-2-2006-1464.The finding was determined to be more than minor because it affected theconfiguration control attribute of the initiating events cornerstone objective to limit
  shutdown was not challenged. The cause of the finding is related to the
the likelihood of those events that upset plant stability and challenge critical
  crosscutting element of human performance associated with work practices
safety functions during shutdown as well as power operations. Using the
  because the fire watch failed to use error prevention techniques like self
shutdown operations significance determination process, the finding was
  checking and peer checking which would have prevented the event
determined to have very low safety significance because the finding did not
  (Section 1R05).
result in a loss of 2 feet or more of reactor coolant system inventory and did not
* Green. A self-revealing noncited violation of Unit 2 Technical
result in a loss of reactor coolant system inventory while in reduced inventory.  
  Specification 6.4.1.a, Procedures, was identified when an operator failed to
The cause of the finding is related to the crosscutting element of humanperformance associated with work practices because the operator failed to use
  close Valve 2DCH-11, resin sluice header drain valve, when securing from a
error prevention techniques like self checking and peer checking which would
  resin transfer as required by procedure. One week later, while aligning the plant
have prevented the event (Section 1R20).*Green. A self-revealing finding was identified associated with the licensee'spractice of using a hammer to remove the main hook pin on the Unit 2 polar
  for alternate purification with Valve 2DCH-11 being out of position, an
crane. Specifically, the license failure to provide clear guidance and training
  unanticipated loss of approximately 230 gallons of reactor coolant system
resulted in station personnel cold working by the main hook and load cell pins
  inventory occurred. This issue was entered into the licensee's corrective action
and this practice resulted in both pins being deformed and not usable with
  program as Condition Report ANO-2-2006-1464.
reactor vessel level lowered to just below reactor vessel flange level. As a result,
  The finding was determined to be more than minor because it affected the
Unit 2 was exposed to an increased period of elevated likelihood of a loss of
  configuration control attribute of the initiating events cornerstone objective to limit
decay heat removal while the unit remained in a lowered vessel level condition
  the likelihood of those events that upset plant stability and challenge critical
for an additional unplanned 27 hours. This issue was entered into the licensee's
  safety functions during shutdown as well as power operations. Using the
corrective action program as Condition Report ANO-2-2006-1553.The finding was determined to be more than minor because it affected theequipment performance attribute of the initiating events cornerstone objective to
  shutdown operations significance determination process, the finding was
limit the likelihood of those events that upset plant stability and challenge critical
  determined to have very low safety significance because the finding did not
safety functions during shutdown as well as power operations. This finding was
  result in a loss of 2 feet or more of reactor coolant system inventory and did not
determined to be a finding of very low safety significance using the shutdown
  result in a loss of reactor coolant system inventory while in reduced inventory.
operations significance determination process because the event did not involve
  The cause of the finding is related to the crosscutting element of human
a loss of shutdown control or a reduction in mitigation capability which would
  performance associated with work practices because the operator failed to use
have increased the frequency of occurrence of a loss of decay heat removal.  
  error prevention techniques like self checking and peer checking which would
-5-EnclosureThe cause of this finding is relat
  have prevented the event (Section 1R20).
ed to the crosscutting element of humanperformance associated with resources because the training of personnel and
* Green. A self-revealing finding was identified associated with the licensees
procedural guidance available was adequate (Section 1R20).*Green. A self-revealing finding was identified when the Unit 1 main feedwaterPump A tripped, resulting in a plant run back to 40 percent reactor power. The
  practice of using a hammer to remove the main hook pin on the Unit 2 polar
trip occurred due to electromagnetic interference from an air conditioning unit
  crane. Specifically, the license failure to provide clear guidance and training
recently installed on top of the main feedwater pump cabinet. This interference
  resulted in station personnel cold working by the main hook and load cell pins
caused an overspeed trip signal on the digital speed monitor for the main
  and this practice resulted in both pins being deformed and not usable with
feedwater pump turbine when no such actual condition occurred. This issue was
  reactor vessel level lowered to just below reactor vessel flange level. As a result,
entered into the licensee's corrective action program as Condition
  Unit 2 was exposed to an increased period of elevated likelihood of a loss of
Report ANO-1-2006-1399.The finding was determined to be more than minor because it affected thedesign control attribute of the initiating events cornerstone objective to limit the
  decay heat removal while the unit remained in a lowered vessel level condition
likelihood of those events that upset plant stability and challenge critical safety
  for an additional unplanned 27 hours. This issue was entered into the licensee's
functions during shutdown as well as power operations. Using Manual
  corrective action program as Condition Report ANO-2-2006-1553.
Chapter 0609, "Significance Determination Process," Phase 1 Worksheet, the
  The finding was determined to be more than minor because it affected the
finding is determined to have very low safety significance because the condition
  equipment performance attribute of the initiating events cornerstone objective to
only affected the initiating events cornerstone and did not contribute to both the
  limit the likelihood of those events that upset plant stability and challenge critical
likelihood of a reactor trip and the likelihood that mitigation equipment or
  safety functions during shutdown as well as power operations. This finding was
functions will not be available. The finding had crosscutting aspects in the area
  determined to be a finding of very low safety significance using the shutdown
of problem identification and resolution associated with operating experience
  operations significance determination process because the event did not involve
because the licensee's failure to implement and institutionalize OE through
  a loss of shutdown control or a reduction in mitigation capability which would
changes to station processes and procedures (Section 4OA3).Cornerstone: Mitigating Systems*Green. A self-revealing noncited violation of ANO Unit 2 LicenseCondition 2.C.(3)(b), "Fire Protection," was identified for failure of the licensee to
  have increased the frequency of occurrence of a loss of decay heat removal.
maintain the lube oil collection system for Reactor Coolant Pumps C and D in an
                                    -4-                                       Enclosure
operable condition. Specifically, the licensee failed to perform a modification on
 
the motor installed on Reactor Coolant Pump C which resulted in the oil
            The cause of this finding is related to the crosscutting element of human
collection tank and its associated overfill berm being filled with water from the
            performance associated with resources because the training of personnel and
component cooling water system. This issue was entered into the licensee's
            procedural guidance available was adequate (Section 1R20).
corrective action program as Condition Report ANO-2-2006-1407.The finding was determined to be more than minor because it affected theprotection against external factors attribute of the mitigating systems cornerstone
      *     Green. A self-revealing finding was identified when the Unit 1 main feedwater
objective to ensure the availability, reliability, and capability of systems that
            Pump A tripped, resulting in a plant run back to 40 percent reactor power. The
respond to initiating events to prevent undesirable consequences. Using the fire
            trip occurred due to electromagnetic interference from an air conditioning unit
protection significance determination process, the finding is determined to have
            recently installed on top of the main feedwater pump cabinet. This interference
very low safety significance because the condition constituted a low degradation
            caused an overspeed trip signal on the digital speed monitor for the main
of a fire prevention and administrative controls feature (Section 1R15).B.Licensee-Identified Violations
            feedwater pump turbine when no such actual condition occurred. This issue was
None.  
            entered into the licensee's corrective action program as Condition
-6-EnclosureREPORT DETAILSSummary of Plant StatusUnit 1 began the inspection period at 100 percent rated thermal power (RTP) and remainedthere until November 9, 2006, when a trip of the Main Feedwater Pump A occurred due to a
            Report ANO-1-2006-1399.
malfunction associated with the electronic overspeed trip device. The trip resulted in an
            The finding was determined to be more than minor because it affected the
automatic runback to 40 percent RTP. Unit 1 returned to 100 percent RTP on  
            design control attribute of the initiating events cornerstone objective to limit the
November 10 and remained there for the remainder of the inspection period. Unit 2 began the inspection period with the reactor shut down for Refueling Outage 2R18. Following the refueling outage, the Unit 2 reactor achieved criticality on October 27 and main
            likelihood of those events that upset plant stability and challenge critical safety
generator output breakers were closed on October 28. Approximately 67 percent RTP was
            functions during shutdown as well as power operations. Using Manual
            Chapter 0609, Significance Determination Process, Phase 1 Worksheet, the
            finding is determined to have very low safety significance because the condition
            only affected the initiating events cornerstone and did not contribute to both the
            likelihood of a reactor trip and the likelihood that mitigation equipment or
            functions will not be available. The finding had crosscutting aspects in the area
            of problem identification and resolution associated with operating experience
            because the licensees failure to implement and institutionalize OE through
            changes to station processes and procedures (Section 4OA3).
Cornerstone: Mitigating Systems
      *     Green. A self-revealing noncited violation of ANO Unit 2 License
            Condition 2.C.(3)(b), Fire Protection, was identified for failure of the licensee to
            maintain the lube oil collection system for Reactor Coolant Pumps C and D in an
            operable condition. Specifically, the licensee failed to perform a modification on
            the motor installed on Reactor Coolant Pump C which resulted in the oil
            collection tank and its associated overfill berm being filled with water from the
            component cooling water system. This issue was entered into the licensee's
            corrective action program as Condition Report ANO-2-2006-1407.
            The finding was determined to be more than minor because it affected the
            protection against external factors attribute of the mitigating systems cornerstone
            objective to ensure the availability, reliability, and capability of systems that
            respond to initiating events to prevent undesirable consequences. Using the fire
            protection significance determination process, the finding is determined to have
            very low safety significance because the condition constituted a low degradation
            of a fire prevention and administrative controls feature (Section 1R15).
B.   Licensee-Identified Violations
      None.
                                                -5-                                       Enclosure
 
                                        REPORT DETAILS
Summary of Plant Status
Unit 1 began the inspection period at 100 percent rated thermal power (RTP) and remained
there until November 9, 2006, when a trip of the Main Feedwater Pump A occurred due to a
malfunction associated with the electronic overspeed trip device. The trip resulted in an
automatic runback to 40 percent RTP. Unit 1 returned to 100 percent RTP on
November 10 and remained there for the remainder of the inspection period.
Unit 2 began the inspection period with the reactor shut down for Refueling Outage 2R18.
Following the refueling outage, the Unit 2 reactor achieved criticality on October 27 and main
generator output breakers were closed on October 28. Approximately 67 percent RTP was
achieved on October 30 when the unit performed a Technical Specification (TS) required
achieved on October 30 when the unit performed a Technical Specification (TS) required
shutdown to hot standby in response to a fire in 480-volt Motor-Control Center 2B-53. Unit 2
shutdown to hot standby in response to a fire in 480-volt Motor-Control Center 2B-53. Unit 2
was restarted, and main generator output breakers were closed on November 1. The unit
was restarted, and main generator output breakers were closed on November 1. The unit
achieved 100 percent RTP on November 3 and remained there for the remainder of the
achieved 100 percent RTP on November 3 and remained there for the remainder of the
inspection period.1.REACTOR SAFETYCornerstones: Initiating Events, Mitigating Systems, Barrier Integrity1R01Adverse Weather Protection (71111.01).1Readiness for Impending Adverse Weather ConditionsOn November 30 the inspectors completed a review of the licensee's readiness forimpending adverse weather involving icy weather. The inspectors: (1) reviewed plant
inspection period.
procedures, the Updated Final Safety Analysis Reports (UFSAR), and TSs to ensure
1.     REACTOR SAFETY
that operator actions defined in adverse weather procedures maintained the readiness
        Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity
of essential systems; (2) walked down portions of the below listed two systems to
1R01 Adverse Weather Protection (71111.01)
ensure that adverse weather protection features (heat tracing, space heaters,
.1      Readiness for Impending Adverse Weather Conditions
weatherized enclosures, temporary chillers) were sufficient to support operability,
        On November 30 the inspectors completed a review of the licensee's readiness for
including the ability to perform safe shutdown functions; (3) reviewed maintenance
        impending adverse weather involving icy weather. The inspectors: (1) reviewed plant
records to determine that applicable surveillance requirements were current before the
        procedures, the Updated Final Safety Analysis Reports (UFSAR), and TSs to ensure
anticipated ice storm developed; and (4) reviewed plant modifications, procedure
        that operator actions defined in adverse weather procedures maintained the readiness
revisions, and operator work arounds to determine if recent facility changes challenged
        of essential systems; (2) walked down portions of the below listed two systems to
plant operation.November 30, 2006, Units 1 and 2, offsite electrical distribution systemsDocuments reviewed by the inspectors are listed in the attachment.  
        ensure that adverse weather protection features (heat tracing, space heaters,
The inspectors completed one sample.  
        weatherized enclosures, temporary chillers) were sufficient to support operability,
-7-Enclosure1R02Evaluation of Changes, Tests, or Experiments (71111.02)     a.Inspection ScopeThe inspectors reviewed the effectiveness of the licensee's implementation of changesto the facility structures, systems, and components (SSCs); risk-significant normal and
        including the ability to perform safe shutdown functions; (3) reviewed maintenance
emergency operating procedures; test programs; and the UFSAR in accordance with
        records to determine that applicable surveillance requirements were current before the
10 CFR 50.59, "Changes, Tests, and Experiments.The inspectors reviewed the safety
        anticipated ice storm developed; and (4) reviewed plant modifications, procedure
evaluations performed by the licensee dealing with the Unit 2 pressurizer replacement.  
        revisions, and operator work arounds to determine if recent facility changes challenged
The evaluations were reviewed to verify that licensee personnel had appropriately
        plant operation.
considered the conditions under which the licensee may make changes to the facility or
        C      November 30, 2006, Units 1 and 2, offsite electrical distribution systems
procedures or conduct tests or experiments without prior NRC approval. Procedures,
        Documents reviewed by the inspectors are listed in the attachment.
evaluations, screenings, and applicability determinations reviewed are listed in the
        The inspectors completed one sample.
attachment to this report.     b.FindingsNo findings of significance were identified.1R04Equipment Alignment (71111.04).1Partial WalkdownThe inspectors: (1) walked down portions of the two below listed risk important systemsand reviewed plant procedures and documents to verify that critical portions of the
                                                -6-                                   Enclosure
selected systems were correctly aligned, and (2) compared deficiencies identified during
 
the walkdown to the licensee's UFSAR and corrective action program (CAP) to ensure
1R02 Evaluation of Changes, Tests, or Experiments (71111.02)
problems were being identified and corrected.*October 3, 2006, Unit 1, Emergency Diesel Generator (EDG) K-4A*December 13, 2006, Unit 1, reactor building spray system Train ADocuments reviewed by the inspectors are listed in the attachment.
  a. Inspection Scope
The inspectors completed two samples.     b.FindingsNo findings of significance were identified.1R05Fire Protection (71111.05).1Quarterly InspectionThe inspectors walked down the six below listed plant areas to assess the materialcondition of active and passive fire protection features and their operational lineup and
      The inspectors reviewed the effectiveness of the licensees implementation of changes
readiness. The inspectors: (1) verified that transient combustibles and hot work
      to the facility structures, systems, and components (SSCs); risk-significant normal and
activities were controlled in accordance with plant procedures; (2) observed the
      emergency operating procedures; test programs; and the UFSAR in accordance with
condition of fire detection devices to verify they remained functional; (3) observed fire  
      10 CFR 50.59, Changes, Tests, and Experiments. The inspectors reviewed the safety
-8-Enclosuresuppression systems to verify they remained functional and that access to manualactuators was unobstructed; (4) verified that fire extinguishers and hose stations were
      evaluations performed by the licensee dealing with the Unit 2 pressurizer replacement.
provided at their designated locations and that they were in a satisfactory condition;
      The evaluations were reviewed to verify that licensee personnel had appropriately
(5) verified that passive fire protection features (electrical raceway barriers, fire doors,
      considered the conditions under which the licensee may make changes to the facility or
fire dampers steel fire proofing, penetration seals, and oil collection systems) were in a
      procedures or conduct tests or experiments without prior NRC approval. Procedures,
satisfactory material condition; (6) verified that adequate compensatory measures were
      evaluations, screenings, and applicability determinations reviewed are listed in the
established for degraded or inoperable fire protection features and that the
      attachment to this report.
compensatory measures were commensurate with the significance of the deficiency;
  b. Findings
and (7) reviewed the UFSAR to determine if the licensee identified and corrected fire
      No findings of significance were identified.
protection problems.*September 25, 2006, Unit 2, Fire Zone 2032-K, containment building (south side)
1R04 Equipment Alignment (71111.04)
*October 17, 2006, Unit 1, Fire Zone 98-J, EDG access corridor
.1    Partial Walkdown
*December 13, 2006, Unit 1, Fire Zones 4-EE, 12-EE, and 14-EE, Elevation 317feet of the auxiliary building, west decay heat removal pump room*December 26, 2006, Unit 2, Fire Zone 2040-JJ, access corridor; charging pump;radwaste and boron management system area*December 27, 2006, Unit 1, Fire Zone 67-U, lab and demineralizer access area
      The inspectors: (1) walked down portions of the two below listed risk important systems
*December 27, 2006, Unit 1, Fire Zone 79-U, upper north piping penetration room
      and reviewed plant procedures and documents to verify that critical portions of the
Documents reviewed by the inspectors are listed in the attachment.  
      selected systems were correctly aligned, and (2) compared deficiencies identified during
The inspectors completed six samples.     b.FindingsIntroduction. A self-revealing, Green noncited violation of TS 6.4.1.c was identified forthe licensee's failure to adequately implement their procedure for the control of hot work
      the walkdown to the licensees UFSAR and corrective action program (CAP) to ensure
and ignition sources while performing hot work activities.Description. On September 25, 2006, hot work activities were being performed on theUnit 2 containment sump strainer. A plastic bag was being utilized at a nearby step-off
      problems were being identified and corrected.
pad at the high contamination area boundary as a receptacle for used protective
      *       October 3, 2006, Unit 1, Emergency Diesel Generator (EDG) K-4A
clothing. While torch cutting on the west containment sump strainer door was in
      *       December 13, 2006, Unit 1, reactor building spray system Train A
progress, sparks from the activity caused the plastic bag to ignite. The inspectors
      Documents reviewed by the inspectors are listed in the attachment.
identified the fire to the firewatch, who was in the vicinity. The bag was extinguished by
      The inspectors completed two samples.
smothering soon thereafter by the workers that were involved in the hot work activity.Procedure EN-DC-127, "Control of Hot Work and Ignition Sources," Revision 2, requiresthat combustible material within 35 feet of the work area that could become ignited from
  b. Findings
the hot work shall be removed or protected. Procedure EN-DC-127, Attachment 9.1,
      No findings of significance were identified.
"Hot Work Permit," was issued for this activity and showed that this requirement to be
1R05 Fire Protection (71111.05)
checked off by the hot work supervisor as being completed. The inspectors noted that
.1    Quarterly Inspection
the bag was within 35 feet of the work area and had not been removed.  
      The inspectors walked down the six below listed plant areas to assess the material
-9-EnclosureCorrective actions that were taken by the licensee in response to this event to preventrecurrence included: moving the step-off pad farther away from the work area, clearing
      condition of active and passive fire protection features and their operational lineup and
      readiness. The inspectors: (1) verified that transient combustibles and hot work
      activities were controlled in accordance with plant procedures; (2) observed the
      condition of fire detection devices to verify they remained functional; (3) observed fire
                                                -7-                                     Enclosure
 
  suppression systems to verify they remained functional and that access to manual
  actuators was unobstructed; (4) verified that fire extinguishers and hose stations were
  provided at their designated locations and that they were in a satisfactory condition;
  (5) verified that passive fire protection features (electrical raceway barriers, fire doors,
  fire dampers steel fire proofing, penetration seals, and oil collection systems) were in a
  satisfactory material condition; (6) verified that adequate compensatory measures were
  established for degraded or inoperable fire protection features and that the
  compensatory measures were commensurate with the significance of the deficiency;
  and (7) reviewed the UFSAR to determine if the licensee identified and corrected fire
  protection problems.
  *       September 25, 2006, Unit 2, Fire Zone 2032-K, containment building (south side)
  *       October 17, 2006, Unit 1, Fire Zone 98-J, EDG access corridor
  *       December 13, 2006, Unit 1, Fire Zones 4-EE, 12-EE, and 14-EE, Elevation 317
            feet of the auxiliary building, west decay heat removal pump room
  *       December 26, 2006, Unit 2, Fire Zone 2040-JJ, access corridor; charging pump;
            radwaste and boron management system area
  *       December 27, 2006, Unit 1, Fire Zone 67-U, lab and demineralizer access area
  *       December 27, 2006, Unit 1, Fire Zone 79-U, upper north piping penetration room
  Documents reviewed by the inspectors are listed in the attachment.
  The inspectors completed six samples.
b. Findings
  Introduction. A self-revealing, Green noncited violation of TS 6.4.1.c was identified for
  the licensees failure to adequately implement their procedure for the control of hot work
  and ignition sources while performing hot work activities.
  Description. On September 25, 2006, hot work activities were being performed on the
  Unit 2 containment sump strainer. A plastic bag was being utilized at a nearby step-off
  pad at the high contamination area boundary as a receptacle for used protective
  clothing. While torch cutting on the west containment sump strainer door was in
  progress, sparks from the activity caused the plastic bag to ignite. The inspectors
  identified the fire to the firewatch, who was in the vicinity. The bag was extinguished by
  smothering soon thereafter by the workers that were involved in the hot work activity.
  Procedure EN-DC-127, Control of Hot Work and Ignition Sources, Revision 2, requires
  that combustible material within 35 feet of the work area that could become ignited from
  the hot work shall be removed or protected. Procedure EN-DC-127, Attachment 9.1,
  Hot Work Permit, was issued for this activity and showed that this requirement to be
  checked off by the hot work supervisor as being completed. The inspectors noted that
  the bag was within 35 feet of the work area and had not been removed.
                                              -8-                                       Enclosure
 
Corrective actions that were taken by the licensee in response to this event to prevent
recurrence included: moving the step-off pad farther away from the work area, clearing
the area near the door of unnecessary equipment and materials, coaching the firewatch
the area near the door of unnecessary equipment and materials, coaching the firewatch
and his supervisor concerning the responsibility of the firewatch and how to deal with
and his supervisor concerning the responsibility of the firewatch and how to deal with
distractions, discussing alternatives to more effectively contain sparks from the cuttingoperation, discussing the event with craft personnel, and conducting more frequent area
distractions, discussing alternatives to more effectively contain sparks from the cutting
inspections.A number of additional deficiencies were identified through a review of recent licenseeperformance in the conduct of related hot work activities. Section 4OA2 of this
operation, discussing the event with craft personnel, and conducting more frequent area
inspections.
A number of additional deficiencies were identified through a review of recent licensee
performance in the conduct of related hot work activities. Section 4OA2 of this
enclosure contains some details of other instances that occurred during the Unit 2
enclosure contains some details of other instances that occurred during the Unit 2
Refueling Outage 2R18. Also, three examples involving circumstances similar to the
Refueling Outage 2R18. Also, three examples involving circumstances similar to the
subject of this finding occurred during the prior refueling outages for each of the two
subject of this finding occurred during the prior refueling outages for each of the two
units. On March 25, 2005, fallen welding slag caused the smoldering of debris below
units. On March 25, 2005, fallen welding slag caused the smoldering of debris below
Containment Cooler D inside the Unit 2 containment building. On September 29 torch
Containment Cooler D inside the Unit 2 containment building. On September 29 torch
cutting resulted in falling hot metal and slag that caused combustible materials in the
cutting resulted in falling hot metal and slag that caused combustible materials in the
work area to catch on fire. On October 14 three small fires of trash bags containing
work area to catch on fire. On October 14 three small fires of trash bags containing
combustible materials in the Unit 1 turbine building basement were caused by hot work
combustible materials in the Unit 1 turbine building basement were caused by hot work
activities that were being performed on the levels above. There was no firewatch posted
activities that were being performed on the levels above. There was no firewatch posted
on the basement level.Each of these instances was entered into the licensee's CAP. These occurrencesrepresent instances of inadequate implementation of applicable hot work control
on the basement level.
procedures. The inspectors concluded that the recent increase in the number of related
Each of these instances was entered into the licensees CAP. These occurrences
represent instances of inadequate implementation of applicable hot work control
procedures. The inspectors concluded that the recent increase in the number of related
findings when compared to past occurrences represented a trend which, if left
findings when compared to past occurrences represented a trend which, if left
uncorrected, could become a more significant safety concern in that it could result in a
uncorrected, could become a more significant safety concern in that it could result in a
fire in or near risk important equipment.Analysis. The performance deficiency associated with this finding involved the failure ofmaintenance personnel to adequately implement the licensee's procedure for control of
fire in or near risk important equipment.
hot work and ignition sources. The finding is greater than minor because it is
Analysis. The performance deficiency associated with this finding involved the failure of
maintenance personnel to adequately implement the licensees procedure for control of
hot work and ignition sources. The finding is greater than minor because it is
associated with the protection against external factors attribute of the initiating events
associated with the protection against external factors attribute of the initiating events
cornerstone, and affects the cornerstone objective to limit the likelihood of those events
cornerstone, and affects the cornerstone objective to limit the likelihood of those events
that upset plant stability and challenge critical safety functions during shutdown as well
that upset plant stability and challenge critical safety functions during shutdown as well
as power operations. Additionally, if left uncorrected, the practice of conducting hot
as power operations. Additionally, if left uncorrected, the practice of conducting hot
work in a manner that results in unintended combustion of nearby materials would
work in a manner that results in unintended combustion of nearby materials would
become a more significant safety concern in that it could result in a fire in or near risk
become a more significant safety concern in that it could result in a fire in or near risk
important equipment. Manual Chapter (MC) 0609, "Significance Determination
important equipment. Manual Chapter (MC) 0609, Significance Determination
Process," Appendix F, "Fire Protection Significance Determination Process," does not
Process, Appendix F, Fire Protection Significance Determination Process, does not
address the potential risk significance of shutdown fire protection findings. Additionally,
address the potential risk significance of shutdown fire protection findings. Additionally,
MC 0609, Appendix G, "Shutdown Operations Significance Determination Process,"
MC 0609, Appendix G, Shutdown Operations Significance Determination Process,
does not address fire protection findings. Thus, the finding is not suitable for
does not address fire protection findings. Thus, the finding is not suitable for
significance determination process evaluation, but has been reviewed by NRC
significance determination process evaluation, but has been reviewed by NRC
management and is determined to be of very low safety significance because the finding
management and is determined to be of very low safety significance because the finding
occurred while the unit was already in a cold shutdown condition; and the operability of
occurred while the unit was already in a cold shutdown condition; and the operability of
equipment necessary to maintain safe shutdown was not challenged. The cause of the
equipment necessary to maintain safe shutdown was not challenged. The cause of the
finding is related to the crosscutting element of human performance in that maintenancepersonnel failed to follow procedures.  
finding is related to the crosscutting element of human performance in that maintenance
-10-EnclosureEnforcement. Unit 2 TS 6.4, "Procedures," requires that written procedures beestablished, implemented, and maintained covering fire protection program
personnel failed to follow procedures.
implementation. Procedure EN-DC-127, "Control of Hot Work and Ignition Sources," is
                                          -9-                                       Enclosure
one of those procedures and requires that combustible material within 35 feet of the
 
work area that could become ignited from the hot work shall be removed or protected.  
    Enforcement. Unit 2 TS 6.4, Procedures, requires that written procedures be
Contrary to this, on September 25, 2006, maintenance personnel failed to remove or
    established, implemented, and maintained covering fire protection program
protect combustible material within 35 feet of the work area. Because the finding is of
    implementation. Procedure EN-DC-127, Control of Hot Work and Ignition Sources, is
very low safety significance and has been entered into the licensee's CAP as Condition
    one of those procedures and requires that combustible material within 35 feet of the
Reports (CRs) ANO-2-2006-1565 and CR ANO-2-2006-1701, this violation is being
    work area that could become ignited from the hot work shall be removed or protected.
treated as an NCV consistent with Section VIA of the Enforcement Policy:
    Contrary to this, on September 25, 2006, maintenance personnel failed to remove or
NCV 05000368/2006005-01, "Fire During Hot Work Activities on the Containment Sump
    protect combustible material within 35 feet of the work area. Because the finding is of
Strainer."1R07Heat Sink Performance (71111.07)     a.Inspection ScopeThe inspectors reviewed licensee programs, verified performance against industrystandards, and reviewed critical operating parameters and maintenance records for the
    very low safety significance and has been entered into the licensees CAP as Condition
Unit 1 EDG A cooling water heat exchanger. The inspectors verified that:  
    Reports (CRs) ANO-2-2006-1565 and CR ANO-2-2006-1701, this violation is being
(1) performance tests were satisfactorily conducted for heat enchanters/heat sinks and
    treated as an NCV consistent with Section VIA of the Enforcement Policy:
reviewed for problems or errors; (2) the licensee utilized the periodic maintenance
    NCV 05000368/2006005-01, Fire During Hot Work Activities on the Containment Sump
method outlined in EPRI NP-7552, "Heat Exchanger Performance Monitoring
    Strainer.
Guidelines"; (3) the licensee properly utilized befalling controls; (4) the licensee's heat
1R07 Heat Sink Performance (71111.07)
exchanger inspections adequately assessed the state of cleanliness of their tubes; and
  a. Inspection Scope
(5) the heat exchanger was correctly categorized under the Maintenance Rule.*September 5, 2006, Unit 1 EDG A cooling water heat exchanger
    The inspectors reviewed licensee programs, verified performance against industry
Documents reviewed by the inspectors are listed in the attachment.
    standards, and reviewed critical operating parameters and maintenance records for the
The inspectors completed one sample.     b.FindingsNo findings of significance were identified.1R08Inservice Inspection Activities (71111.08)Inspection Procedure 71111.08 requires four samples size as identified inSections 02.01, 02.02, 02.03, and 02.04.  
    Unit 1 EDG A cooling water heat exchanger. The inspectors verified that:
-11-Enclosure     a.Inspection Scope.1Performance of Nondestructive Examination (NDE) Activities Other than SteamGenerator Tube Inspections, Pressurized Water Reactor (PWR) Vessel Upper HeadPenetration Inspections, Boric Acid Corrosion ControlThe inspection procedure requires the review of NDE activities consisting of two or threedifferent types (i.e., volumetric, surface, or visual). The inspectors observed the
    (1) performance tests were satisfactorily conducted for heat enchanters/heat sinks and
performance of three ultrasonic examinations (volumetric) (one on a section of service
    reviewed for problems or errors; (2) the licensee utilized the periodic maintenance
water piping for wall thickness and two on field welds in the pressurizer spray line). The
    method outlined in EPRI NP-7552, Heat Exchanger Performance Monitoring
inspectors also reviewed the radiographic examinations (volumetric) of the two spray
    Guidelines; (3) the licensee properly utilized befalling controls; (4) the licensees heat
line welds. (The welds are identified in the attachment to this report.) For each of the observed NDE activities, the inspectors verified that the examinationswere performed in accordance with the specific site procedures and the applicable
    exchanger inspections adequately assessed the state of cleanliness of their tubes; and
American Society of Mechanical Engineers Boiler and Pressure Vessel Code (ASME
    (5) the heat exchanger was correctly categorized under the Maintenance Rule.
Code) requirements.During review of each examination, the inspectors verified that appropriateNDE procedures were used, examinations and conditions were as specified in the
    *       September 5, 2006, Unit 1 EDG A cooling water heat exchanger
procedure, and test instrumentation or equipment was properly calibrated and within the
    Documents reviewed by the inspectors are listed in the attachment.
allowable calibration period. The inspectors also verified the NDE certifications of the
    The inspectors completed one sample.
personnel who performed the above volumetric examinations. Finally, the inspectors
  b. Findings
observed that indications identified during the radiographic examinations weredispositioned in accordance with the ASME Code-qualified NDE procedures used to
    No findings of significance were identified.
perform the examinations.The inspection procedure requires review of one or two examinations with recordableindications that were accepted for continued service to ensure that the disposition was
1R08 Inservice Inspection Activities (71111.08)
made in accordance with the ASME Code. The inspectors were informed that no
    Inspection Procedure 71111.08 requires four samples size as identified in
indications exceeding ASME Code allowables were known to be in service.The inspection procedure further requires verification of one to three welds on Class 1or 2 pressure boundary piping to ensure that the welding process and welding
    Sections 02.01, 02.02, 02.03, and 02.04.
examinations were performed in accordance with the ASME Code. The inspectors
                                            -10-                                       Enclosure
observed welding performed on a safety injection system valve in the prefabrication
 
shop. The inspectors verified that the welding was performed in accordance with
  a. Inspection Scope
Sections IX and XI of the ASME Code. This included review of welding material issue
.1    Performance of Nondestructive Examination (NDE) Activities Other than Steam
slips to establish that the appropriate welding materials had been used and verification
      Generator Tube Inspections, Pressurized Water Reactor (PWR) Vessel Upper Head
that the welding procedure specification (WPS E-P8-T-A8,Ar, "Manual Gas Tungsten
      Penetration Inspections, Boric Acid Corrosion Control
Arc Welding (GTAW) of P-No. 8 Stainless Steels," Revision 0) had been properly
      The inspection procedure requires the review of NDE activities consisting of two or three
qualified.The inspectors completed the one sample required by Section 02.01..2Reactor Vessel Upper Head Penetration Inspection ActivitiesThe inspection requirements for this section parallel the inspection requirement steps inSection 02.01. The inspectors observed the NDEs on nine reactor vessel upper head  
      different types (i.e., volumetric, surface, or visual). The inspectors observed the
-12-Enclosurepenetrations. There were eight control element drive mechanism penetrations (Nos. 12,21, 58, 59, 60, 61, 72, and 79) and one incore instrumentation penetration (No. 82).The inspectors verified that the nondestructive activities were performed in accordancewith the requirements of NRC Order EA-03-009. The NDEs performed during the NRC
      performance of three ultrasonic examinations (volumetric) (one on a section of service
inspection did not reveal any defects or indications. The inspectors completed the one sample required by Section 02.02..3Boric Acid Corrosion Control Inspection Activities (PWRs)The inspectors evaluated the implementation of the licensee's boric acid corrosioncontrol program for monitoring degradation of those systems that could be deleteriously
      water piping for wall thickness and two on field welds in the pressurizer spray line). The
affected by boric acid corrosion. The inspection procedure requires review of a sample
      inspectors also reviewed the radiographic examinations (volumetric) of the two spray
of boric acid corrosion control walkdown visual examination activities through either
      line welds. (The welds are identified in the attachment to this report.)
direct observation or record review. The inspectors reviewed the documentation
      For each of the observed NDE activities, the inspectors verified that the examinations
associated with the licensee's boric acid corrosion control walkdown. Additionally, the
      were performed in accordance with the specific site procedures and the applicable
inspectors performed independent observations of piping containing boric acid during
      American Society of Mechanical Engineers Boiler and Pressure Vessel Code (ASME
walkdowns of the containment building and the auxiliary building. The inspection procedure requires verification that visual inspections emphasizelocations where boric acid leaks can cause degradation of safety significant
      Code) requirements.
components. The inspectors verified through direct observation and program/record
      During review of each examination, the inspectors verified that appropriate
review that the licensee's boric acid corrosion control inspection efforts are directed
      NDE procedures were used, examinations and conditions were as specified in the
towards locations where boric acid leaks can cause degradation of safety-related
      procedure, and test instrumentation or equipment was properly calibrated and within the
components.The inspection procedure requires both a review of one to three engineering evaluationsperformed for boric acid leaks found on reactor coolant system (RCS) piping and
      allowable calibration period. The inspectors also verified the NDE certifications of the
components and one to three corrective actions performed for identified boric acid
      personnel who performed the above volumetric examinations. Finally, the inspectors
leaks. The licensee had identified a boric acid leak on the containment spray header
      observed that indications identified during the radiographic examinations were
during an inspection for materials that could come loose and clog the sump screens
      dispositioned in accordance with the ASME Code-qualified NDE procedures used to
during a loss-of-coolant accident or steam line rupture inside containment. The
      perform the examinations.
inspectors reviewed the licensee's analysis of the condition to evaluate the assessment
      The inspection procedure requires review of one or two examinations with recordable
of the condition and proposed corrective actions.The inspectors completed the one sample required by Section 02.03..4Steam Generator Tube Inspection ActivitiesThere were no steam generator tube inspections performed during this outage. Theinspectors reviewed Evaluation ER-2005-0469-001, "Operational Assessment of ANO-2
      indications that were accepted for continued service to ensure that the disposition was
Steam Generator Tubing for Cycles 18-20," dated August 31, 2006. The evaluation
      made in accordance with the ASME Code. The inspectors were informed that no
concluded that no tube examinations were required to be performed during
      indications exceeding ASME Code allowables were known to be in service.
Cycles 18-20. The inspectors noted that the basis was the condition of the tubes from
      The inspection procedure further requires verification of one to three welds on Class 1
the previous inspections that were performed after the steam generators were replaced.This sample was not completed because there was no activity to observe.  
      or 2 pressure boundary piping to ensure that the welding process and welding
-13-Enclosure.5Identification and Resolution of ProblemsThe inspection procedure requires review of a sample of problems associated withinservice inspections documented by the licensee in the CAP for appropriateness of the
      examinations were performed in accordance with the ASME Code. The inspectors
corrective actions. The inspectors reviewed three CRs, which dealt with inservice
      observed welding performed on a safety injection system valve in the prefabrication
inspection and welding activities. From this review, the inspectors concluded that the
      shop. The inspectors verified that the welding was performed in accordance with
licensee has an appropriate threshold for entering issues into the CAP and has
      Sections IX and XI of the ASME Code. This included review of welding material issue
procedures that direct a root cause evaluation when necessary. The licensee also had
      slips to establish that the appropriate welding materials had been used and verification
an effective program for applying industry operating experience.     b.FindingsNo findings of significance were identified.1R11Licensed Operator Requalification Program (71111.11)     a.Inspection ScopeOn December 14, 2006, the inspectors observed testing and training of Unit 1 seniorreactor operators and reactor operators to identify deficiencies and discrepancies in the
      that the welding procedure specification (WPS E-P8-T-A8,Ar, Manual Gas Tungsten
training, to assess operator performance, and to assess the evaluator's critique. The
      Arc Welding (GTAW) of P-No. 8 Stainless Steels, Revision 0) had been properly
training was a simulator training scenario.Documents reviewed by the inspectors included:
      qualified.
*ANO Unit 1 Dynamic Exam Scenario SES-1-008, Revision 5
      The inspectors completed the one sample required by Section 02.01.
The inspectors completed one sample.     b.FindingsNo findings of significance were identified.1R12Maintenance Effectiveness (71111.12)     a.Inspection ScopeThe inspectors reviewed the two below listed maintenance activities to: (1) verify theappropriate handling of SSCs performance or condition problems; (2) verify the
.2    Reactor Vessel Upper Head Penetration Inspection Activities
appropriate handling of degraded SSC functional performance; (3) evaluate the role of
      The inspection requirements for this section parallel the inspection requirement steps in
work practices and common cause problems; and (4) evaluate the handling of SSC
      Section 02.01. The inspectors observed the NDEs on nine reactor vessel upper head
issues reviewed under the requirements of the Maintenance Rule, 10 CFR Part 50,
                                                -11-                                   Enclosure
Appendix B, and TSs. *November 28, 2006, Unit 1, turbine building ventilation*December 5, 2006, Unit 2, 480-volt electrical distributionDocuments reviewed by the inspectors are listed in the attachment.
 
-14-EnclosureThe inspectors completed two samples.     b.FindingsNo findings of significance were identified.1R13Maintenance Risk Assessments and Emergent Work Control (71111.13).1Risk Assessment and Management of Risk     a.Inspection ScopeRisk Assessment and Management of RiskThe inspectors reviewed the six below listed assessment activities to verify: (1) performance of risk assessments when required by 10 CFR 50.65 (a)(4) and
  penetrations. There were eight control element drive mechanism penetrations (Nos. 12,
licensee procedures prior to changes in plant configuration for maintenance activities
  21, 58, 59, 60, 61, 72, and 79) and one incore instrumentation penetration (No. 82).
and plant operations; (2) the accuracy, adequacy, and completeness of the information
  The inspectors verified that the nondestructive activities were performed in accordance
considered in the risk assessment; (3) that the licensee recognizes, and/or enters as
  with the requirements of NRC Order EA-03-009. The NDEs performed during the NRC
applicable, the appropriate licensee-established risk category according to the risk
  inspection did not reveal any defects or indications.
assessment results and licensee procedures; and (4) that the licensee identified and
  The inspectors completed the one sample required by Section 02.02.
corrected problems related to maintenance risk assessments.*September 19 through October 27, 2006, Unit 2, pressurizer replacement
.3 Boric Acid Corrosion Control Inspection Activities (PWRs)
*September 19 through October 27, 2006, Unit 2, containment sump modification
  The inspectors evaluated the implementation of the licensees boric acid corrosion
*November 13-17, 2006, Unit 1, planned maintenance for the week
  control program for monitoring degradation of those systems that could be deleteriously
*November 27 through December 1, 2006, Unit 1, planned maintenance for theweek*December 4-8, 2006, Unit 2, planned maintenance for the week
  affected by boric acid corrosion. The inspection procedure requires review of a sample
*December 11-15, 2006, Unit 1, planned maintenance for the week
  of boric acid corrosion control walkdown visual examination activities through either
Documents reviewed by the inspectors are listed in the attachment.
  direct observation or record review. The inspectors reviewed the documentation
The inspectors completed six samples.     b.FindingsNo findings of significance were identified.  
  associated with the licensees boric acid corrosion control walkdown. Additionally, the
-15-Enclosure1R15Operability Evaluations (71111.15)     a.Inspection ScopeThe inspectors: (1) reviewed plants status documents, such as operator shift logs,emergent work documentation, deferred modifications, and standing orders, to
  inspectors performed independent observations of piping containing boric acid during
determine if an operability evaluation was warranted for degraded components;
  walkdowns of the containment building and the auxiliary building.
(2) referred to the UFSAR and design basis documents to review the technical
  The inspection procedure requires verification that visual inspections emphasize
adequacy of licensee operability evaluations; (3) evaluated compensatory measures
  locations where boric acid leaks can cause degradation of safety significant
associated with operability evaluations; (4) determined degraded component impact on
  components. The inspectors verified through direct observation and program/record
any TSs; (5) used the significance determination process to evaluate the risk
  review that the licensees boric acid corrosion control inspection efforts are directed
significance of degraded or inoperable equipment; and (6) verified that the licensee has
  towards locations where boric acid leaks can cause degradation of safety-related
identified and implemented appropriate corrective actions associated with degraded
  components.
components.*September 22, 2006, Unit 2, reactor coolant pump (RCP) oil collection system*October 3, 2006, Unit 2, Electrical Bus 2B-5
  The inspection procedure requires both a review of one to three engineering evaluations
*October 28, 2006, Unit 2, containment spray header
  performed for boric acid leaks found on reactor coolant system (RCS) piping and
*December 19, 2006, Unit 2, containment sumpDocuments reviewed by the inspectors are listed in the attachment.
  components and one to three corrective actions performed for identified boric acid
The inspectors completed four samples.     b.FindingsIntroduction. A Green self-revealing noncited violation of the Unit 2 license condition forfire protection was identified for failure of the licensee to maintain the RCP oil collection
  leaks. The licensee had identified a boric acid leak on the containment spray header
system for RCPs C and D in an operable condition. Specifically, the licensee failed to
  during an inspection for materials that could come loose and clog the sump screens
perform a modification on the motor installed on RCP C, which resulted in the oil
  during a loss-of-coolant accident or steam line rupture inside containment. The
collection tank and its associated overfill berm filling up and overflowing with water from
  inspectors reviewed the licensees analysis of the condition to evaluate the assessment
the component cooling water (CCW) system. Description. On September 20, 2006, while the licensee was conducting a hotshutdown walkdown in containment during the start of Refueling Outage 2R18, the
  of the condition and proposed corrective actions.
licensee discovered that the RCP oil collection system drain tank for RCPs C and D,
  The inspectors completed the one sample required by Section 02.03.
(2T-110) and its associated overfill berm were filled and overflowing with water. The
.4 Steam Generator Tube Inspection Activities
licensee determined that the drain tank and associated berm were inoperable because
  There were no steam generator tube inspections performed during this outage. The
the licensee could not perform their intended function of providing a collection and
  inspectors reviewed Evaluation ER-2005-0469-001, Operational Assessment of ANO-2
holding point for possible oil leakage from RCPs C and D. The licensee obtained a sample of the water and determined that it was from the CCWsystem. Based on this, the licensee then identified and performed inspections of all
  Steam Generator Tubing for Cycles 18-20, dated August 31, 2006. The evaluation
interface points of the CCW system with the RCP oil collection system. During this
  concluded that no tube examinations were required to be performed during
inspection, two leakage points were identified: the outlet flange of lube oil
  Cycles 18-20. The inspectors noted that the basis was the condition of the tubes from
Cooler 2E-25D, and the interface of the threaded supply and return piping nipples forthe lower bearing oil cooler on RCP C. The leakage from the lower bearing oil cooler
  the previous inspections that were performed after the steam generators were replaced.
was determined to be the source that was leaking into the oil collection system through
  This sample was not completed because there was no activity to observe.
the drip pans below the motor.  
                                          -12-                                       Enclosure
-16-EnclosureDuring their investigation to determine the cause of this failure, the licensee identifiedthe cause of the leakage to be fatigue at the root diameter of the threaded schedule
 
40 pipe nipple. They also determined that this type of failure had previously occurred on
.5    Identification and Resolution of Problems
the motor installed on RCP B in December of 1995. This failure was documented in
      The inspection procedure requires review of a sample of problems associated with
      inservice inspections documented by the licensee in the CAP for appropriateness of the
      corrective actions. The inspectors reviewed three CRs, which dealt with inservice
      inspection and welding activities. From this review, the inspectors concluded that the
      licensee has an appropriate threshold for entering issues into the CAP and has
      procedures that direct a root cause evaluation when necessary. The licensee also had
      an effective program for applying industry operating experience.
  b. Findings
      No findings of significance were identified.
1R11 Licensed Operator Requalification Program (71111.11)
  a. Inspection Scope
      On December 14, 2006, the inspectors observed testing and training of Unit 1 senior
      reactor operators and reactor operators to identify deficiencies and discrepancies in the
      training, to assess operator performance, and to assess the evaluator's critique. The
      training was a simulator training scenario.
      Documents reviewed by the inspectors included:
      *       ANO Unit 1 Dynamic Exam Scenario SES-1-008, Revision 5
      The inspectors completed one sample.
  b. Findings
      No findings of significance were identified.
1R12 Maintenance Effectiveness (71111.12)
  a. Inspection Scope
      The inspectors reviewed the two below listed maintenance activities to: (1) verify the
      appropriate handling of SSCs performance or condition problems; (2) verify the
      appropriate handling of degraded SSC functional performance; (3) evaluate the role of
      work practices and common cause problems; and (4) evaluate the handling of SSC
      issues reviewed under the requirements of the Maintenance Rule, 10 CFR Part 50,
      Appendix B, and TSs.
      *       November 28, 2006, Unit 1, turbine building ventilation
      *       December 5, 2006, Unit 2, 480-volt electrical distribution
      Documents reviewed by the inspectors are listed in the attachment.
                                              -13-                                   Enclosure
 
      The inspectors completed two samples.
  b. Findings
      No findings of significance were identified.
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)
.1    Risk Assessment and Management of Risk
  a. Inspection Scope
      Risk Assessment and Management of Risk
      The inspectors reviewed the six below listed assessment activities to verify:
      (1) performance of risk assessments when required by 10 CFR 50.65 (a)(4) and
      licensee procedures prior to changes in plant configuration for maintenance activities
      and plant operations; (2) the accuracy, adequacy, and completeness of the information
      considered in the risk assessment; (3) that the licensee recognizes, and/or enters as
      applicable, the appropriate licensee-established risk category according to the risk
      assessment results and licensee procedures; and (4) that the licensee identified and
      corrected problems related to maintenance risk assessments.
      *       September 19 through October 27, 2006, Unit 2, pressurizer replacement
      *       September 19 through October 27, 2006, Unit 2, containment sump modification
      *       November 13-17, 2006, Unit 1, planned maintenance for the week
      *       November 27 through December 1, 2006, Unit 1, planned maintenance for the
              week
      *       December 4-8, 2006, Unit 2, planned maintenance for the week
      *       December 11-15, 2006, Unit 1, planned maintenance for the week
      Documents reviewed by the inspectors are listed in the attachment.
      The inspectors completed six samples.
  b. Findings
      No findings of significance were identified.
                                              -14-                                   Enclosure
 
1R15 Operability Evaluations (71111.15)
  a. Inspection Scope
    The inspectors: (1) reviewed plants status documents, such as operator shift logs,
    emergent work documentation, deferred modifications, and standing orders, to
    determine if an operability evaluation was warranted for degraded components;
    (2) referred to the UFSAR and design basis documents to review the technical
    adequacy of licensee operability evaluations; (3) evaluated compensatory measures
    associated with operability evaluations; (4) determined degraded component impact on
    any TSs; (5) used the significance determination process to evaluate the risk
    significance of degraded or inoperable equipment; and (6) verified that the licensee has
    identified and implemented appropriate corrective actions associated with degraded
    components.
    *       September 22, 2006, Unit 2, reactor coolant pump (RCP) oil collection system
    *       October 3, 2006, Unit 2, Electrical Bus 2B-5
    *       October 28, 2006, Unit 2, containment spray header
    *       December 19, 2006, Unit 2, containment sump
    Documents reviewed by the inspectors are listed in the attachment.
    The inspectors completed four samples.
  b. Findings
    Introduction. A Green self-revealing noncited violation of the Unit 2 license condition for
    fire protection was identified for failure of the licensee to maintain the RCP oil collection
    system for RCPs C and D in an operable condition. Specifically, the licensee failed to
    perform a modification on the motor installed on RCP C, which resulted in the oil
    collection tank and its associated overfill berm filling up and overflowing with water from
    the component cooling water (CCW) system.
    Description. On September 20, 2006, while the licensee was conducting a hot
    shutdown walkdown in containment during the start of Refueling Outage 2R18, the
    licensee discovered that the RCP oil collection system drain tank for RCPs C and D,
    (2T-110) and its associated overfill berm were filled and overflowing with water. The
    licensee determined that the drain tank and associated berm were inoperable because
    the licensee could not perform their intended function of providing a collection and
    holding point for possible oil leakage from RCPs C and D.
    The licensee obtained a sample of the water and determined that it was from the CCW
    system. Based on this, the licensee then identified and performed inspections of all
    interface points of the CCW system with the RCP oil collection system. During this
    inspection, two leakage points were identified: the outlet flange of lube oil
    Cooler 2E-25D, and the interface of the threaded supply and return piping nipples for
    the lower bearing oil cooler on RCP C. The leakage from the lower bearing oil cooler
    was determined to be the source that was leaking into the oil collection system through
    the drip pans below the motor.
                                                -15-                                     Enclosure
 
During their investigation to determine the cause of this failure, the licensee identified
the cause of the leakage to be fatigue at the root diameter of the threaded schedule
40 pipe nipple. They also determined that this type of failure had previously occurred on
the motor installed on RCP B in December of 1995. This failure was documented in
CR ANO-2-1995-0555 and was also determined to be due to fatigue at the root diameter
CR ANO-2-1995-0555 and was also determined to be due to fatigue at the root diameter
of the threaded schedule 40 pipe nipple. The licensee determined, during their review
of the threaded schedule 40 pipe nipple. The licensee determined, during their review
of the RCP B failure of December 1995, that Modification PEAR 9-0330, Revision 1, had
of the RCP B failure of December 1995, that Modification PEAR 9-0330, Revision 1, had
been developed and implemented to replace the schedule 40 threaded pipe nipple on
been developed and implemented to replace the schedule 40 threaded pipe nipple on
the RCPs with schedule 80 threaded pipe nipples. This modification was performed on
the RCPs with schedule 80 threaded pipe nipples. This modification was performed on
the motors of all installed RCPs but not the Unit 2 spare motor. Completion of the
the motors of all installed RCPs but not the Unit 2 spare motor. Completion of the
modification on the spare RCP motor was to be accomplished during motor
modification on the spare RCP motor was to be accomplished during motor
refurbishment; however, the modification was never performed. In 2005 during
refurbishment; however, the modification was never performed. In 2005 during
Refueling Outage 2R17, the spare RCP motor was installed as the RPC C motor without
Refueling Outage 2R17, the spare RCP motor was installed as the RPC C motor without
the modification.In reviewing this issue, the inspectors noted that the licensee had trend data for thevolume of oil in RCPs C and D which indicated that oil volume in RCPs C and D had
the modification.
gone down over the cycle. The inspectors determined through interviews that this oil
In reviewing this issue, the inspectors noted that the licensee had trend data for the
volume of oil in RCPs C and D which indicated that oil volume in RCPs C and D had
gone down over the cycle. The inspectors determined through interviews that this oil
was not contained in the oil collection system or the overflow berm as per design but
was not contained in the oil collection system or the overflow berm as per design but
had most likely overflowed the berm and gone to the containment sump via the floor
had most likely overflowed the berm and gone to the containment sump via the floor
drain system. During the operating cycle, the sump had been pumped to the auxiliary
drain system. During the operating cycle, the sump had been pumped to the auxiliary
building for processing.Analysis. The inspectors determined that the failure to maintain the oil collection systemdrain tank for RCPs C and D in an operable condition was a performance deficiency.  
building for processing.
Analysis. The inspectors determined that the failure to maintain the oil collection system
drain tank for RCPs C and D in an operable condition was a performance deficiency.
The finding was determined to be more than minor because it affected the protection
The finding was determined to be more than minor because it affected the protection
against external factors attribute of the mitigating systems cornerstone objective to
against external factors attribute of the mitigating systems cornerstone objective to
ensure the availability, reliability, and capability of systems that respond to initiating
ensure the availability, reliability, and capability of systems that respond to initiating
events to prevent undesirable consequences. Using MC 0609, "Significance
events to prevent undesirable consequences. Using MC 0609, Significance
Determination Process," Phase 1 Worksheet, the finding is assumed to degrade fire
Determination Process, Phase 1 Worksheet, the finding is assumed to degrade fire
protection defense-in-depth strategies involving barriers; therefore, the significance of
protection defense-in-depth strategies involving barriers; therefore, the significance of
the finding is determined by using Appendix F, "Fire Protection Significance
the finding is determined by using Appendix F, Fire Protection Significance
Determination Process," of MC 0609. Using the Phase 1 Worksheet of Appendix F, the
Determination Process, of MC 0609. Using the Phase 1 Worksheet of Appendix F, the
inspectors assumed the condition represented a low degradation of the fire prevention
inspectors assumed the condition represented a low degradation of the fire prevention
and administrative controls category since the oil collection would have kept oil from
and administrative controls category since the oil collection would have kept oil from
contacting hot surfaces in the containment building. Additionally, the inspectors
contacting hot surfaces in the containment building. Additionally, the inspectors
assumed that no intervening combustibles were present between the overflow path and
assumed that no intervening combustibles were present between the overflow path and
adjacent fire areas and that the containment sump, to which the floor drains installed in
adjacent fire areas and that the containment sump, to which the floor drains installed in
the area of the berm transported any oil that overflowed, lacked a significant ignition
the area of the berm transported any oil that overflowed, lacked a significant ignition
source.
Enforcement. ANO Unit 2 License Condition 2.C.(3)(b), Fire Protection, states, in part,
that the licensee shall implement and maintain all provisions of the approved fire
protection program. ANO Unit 1 and Unit 2 - Fire Hazards Analysis, Revision 9, is part
of the ANO Unit 2 fire protection program. Section 6.4.5, Fire Barriers, Seals, and
Penetrations, of the Fire Hazards Analysis states, in part, that the fire barrier system at
ANO has been designed to ensure that fires will be confined or adequately retarded
from spreading to adjacent portions of the facility. Contrary to this, the filling to overflow
of the oil collection system tank and overflow berm with water from the CCW system
                                          -16-                                      Enclosure
      during Operating Cycle 18 prevented a potential RCP oil fire in the containment
      basement from being confined per the fire protection program. Because the finding is of
      very low safety significance and has been entered into the licensees CAP as
      CR ANO-2-2006-1407, this violation is being treated as an NCV consistent with
      Section VIA of the Enforcement Policy: NCV 05000368/2006005-02, Failure to Perform
      Modification Resulted in an Inoperable RCP Oil Collection System.
1R17 Permanent Plant Modifications (71111.17)
.1    Annual Review
      The inspectors reviewed key affected parameters associated with energy needs,
      materials/replacement components, timing, heat removal, control signals, equipment
      protection from hazards, operations, flowpaths, pressure boundary, ventilation
      boundary, structural, process medium properties, licensing basis, and failure modes for
      the modification listed below. The inspectors verified that: (1) modification preparation,
      staging, and implementation does not impair emergency/abnormal operating procedure
      actions, key safety functions, or operator response to loss of key safety functions;
      (2) postmodification testing maintained the plant in a safe configuration during testing by
      verifying that unintended system interactions will not occur, SSC performance
      characteristics still meet the design basis, the appropriateness of modification design
      assumptions, and the modification test acceptance criteria has been met; and (3) the
      licensee has identified and implemented appropriate corrective actions associated with
      permanent plant modifications.
      *      September 19 through October 26, 2006, Unit 2, pressurizer replacement
1R19 Postmaintenance Testing (71111.19)
  a. Inspection Scope
      The inspectors selected the six below listed postmaintenance test activities of risk
      significant systems or components. For each item, the inspectors: (1) reviewed the
      applicable licensing basis and/or design-basis documents to determine the safety
      functions; (2) evaluated the safety functions that may have been affected by the
      maintenance activity; and (3) reviewed the test procedure to ensure it adequately tested
      the safety function that may have been affected. The inspectors either witnessed or
      reviewed test data to verify that acceptance criteria were met, plant impacts were
      evaluated, test equipment was calibrated, procedures were followed, jumpers were
      properly controlled, the test data results were complete and accurate, the test
      equipment was removed, the system was properly realigned, and deficiencies during
      testing were documented. The inspectors also reviewed the UFSAR to determine if the
      licensee identified and corrected problems related to postmaintenance testing.
      *      October 17, 2006, Unit 1, Emergency Feedwater Pump P-7A
      *      October 22, 2006, Unit 2, pressurizer heater capacity
      *      October 24, 2006, Unit 2, replacement pressurizer relief valve monitor test
                                              -17-                                    Enclosure
      *        October 25, 2006, Unit 2, containment spray header repairs
      *        October 27, 2006, Unit 2, replacement pressurizer leakage
      *        November 1, 2006, Unit 2, containment building personnel hatch leakage rate
              testing
      Documents reviewed by the inspectors are listed in the attachment.
      The inspectors completed six samples.
  b. Findings
      No findings of significance were identified.
1R20 Refueling and Outage Activities (71111.20)
1.    Unit 2 Forced Outage Caused by Fire in Motor Control Center 2B-53
  a. Inspection Scope
      The inspectors reviewed the following risk significant outage activities to verify defense
      in depth commensurate with the outage risk control plan and compliance with the TSs:
      (1) the risk control plan, (2) tagging/clearance activities, (3) heatup and cooldown
      activities, and (4) restart activities.
      The inspectors completed one sample.
  b. Findings
      No findings of significance were identified.
2.    Refueling and Pressurizer Replacement Outage 2R18
  a. Inspection Scope
      The inspectors reviewed the following risk significant refueling items or outage activities
      to verify defense in depth commensurate with the outage risk control plan, compliance
      with the TSs, and adherence to commitments in response to Generic Letter 88-17, Loss
      of Decay Heat Removal: (1) the risk control plan, (2) tagging/clearance activities,
      (3) RCS instrumentation, (4) electrical power, (5) decay heat removal, (6) spent fuel pool
      cooling, (7) inventory control, (8) reactivity control, (9) containment closure, (10) reduced
      inventory conditions, (11) refueling activities, (12) heatup and cooldown activities,
      (13) restart activities, and (14) licensee identification and implementation of appropriate
      corrective actions associated with refueling and outage activities. The inspectors
      containment inspections included observation of the containment sump for damage and
      debris, supports, braces, and snubbers for evidence of excessive stress, water hammer,
      or aging.
                                                -18-                                      Enclosure
      The inspectors completed one sample.
  b. Findings
.1    Inadvertent RCS Draining While in Mode 5
      Introduction. A Green self-revealing noncited violation of the licensees TS requirement
      for procedures was identified when an operator failed to close a resin sluice header
      drain valve as required by procedure. Later, while operators were aligning the unit for
      alternate reactor coolant purification, a loss of approximately 230 gallons of RCS
      inventory occurred.
      Description. On September 14, 2006, operations personnel performed
      Procedure OP-2104.019, Clean Resin Transfer, to add clean resin to Purification Ion
      Exchanger 2T-36B. During this procedure, Valve 2DCH-11 was opened as part of the
      system lineup. Subsequently, when the evolution was completed and the plant lineup
      was being restored, station personnel failed to properly perform Step 22.2 of the
      procedure leaving Valve 2DCH-11 in the open position.
      Subsequently, on September 21, 2006, with Unit 2 in Mode 5, the licensee was in the
      process of aligning alternate purification in accordance with Procedure OP-2104.004,
      Shutdown Cooling System, Attachment J, Alternate Purification. When Step 2.11 of
      this procedure was performed, the control room operators noted that pressurizer level
      began to lower. The evolution was stopped and the lineup was secured. At this point,
      pressurizer level stopped lowering. Station personnel performed a system walkdown
      and discovered that Valve 2DCH-11 was in the open position. Operations personnel
      determined that approximately 230 gallons were drained from the RCS through the open
      valve.
      During their review, the inspectors noted that Procedure OP-2104.004, Attachment J,
      directed personnel to prepare a caution tag for components to prevent the loss of RCS
      inventory. However, the procedure contained a note that preceded Step 1.11 which
      directed the caution tag be hung on the room door instead of Valve 2DCH-11 and two
      other valves. This tag stated that, since the valves were normally closed, any
      misalignment would be detected by system abnormalities. The inspectors determined
      that this note contributed to Valve 2DCH-11 not being discovered out of position prior to
      initiating alternate purification since the licensee did not perform a valve lineup
      verification.
      Analysis. The failure of station personnel to manipulate Valve 2DCH-11 in accordance
      with station procedure was determined to be a performance deficiency. The finding was
      determined to be more than minor because it affected the configuration control attribute
      of the initiating events cornerstone objective to limit the likelihood of those events that
      upset plant stability and challenge critical safety functions during shutdown as well as
      power operations. The inspectors used MC 0609, Significance Determination Process,
      Appendix G, Shutdown Operations Significance Determination Process, and assumed
      that the administrative controls implemented to avoid operations that could lead to
      perturbations in RCS level control attribute was affected. The finding was determined to
      have very low safety significance because the finding did not result in a loss of 2 feet or
                                                -19-                                    Enclosure
  more of RCS inventory and did not result in a loss of RCS inventory while the unit was in
  reduced inventory. The cause of the finding is related to the crosscutting aspect of
  human performance associated with work practices because the operator failed to use
  error prevention techniques like self checking and peer checking which would have
  prevented the event.
  Enforcement. Unit 2 TS, Section 6.4.1.a, Procedures, requires, in part, that written
  procedures shall be established, implemented, and maintained covering the applicable
  procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A,
  February 1978. Procedure OP-2104.019, Clean Resin Transfer, is a procedure
  required by Regulatory Guide 1.33. Contrary to the above, on September 14, 2006, the
  licensee failed to fully implement Procedure OP-2104.019, Clean Resin Transfer,
  when the licensee failed to close Valve 2DCH-11. Because this finding is of very low
  safety significance and has been entered into the CAP as CR ANO-2-2006-1464, this
  violation is being treated as an NCV, consistent with Section VIA of the NRC
  Enforcement Policy: NCV 05000368/2006005-03, Inadvertent RCS Draining While in
  Mode 5.
.2 Unplanned Increase in Time with Reactor Vessel Water Level at Flange Level
  Introduction. A Green self-revealing finding was identified associated with the licensees
  use of a hammer to remove and reinstall both the main hook pin and the load cell pin on
  the Unit 2 polar crane. Unit 2 was maintained in a condition with reactor vessel water
  level being maintained just below the reactor vessel flange for an additional unplanned
  27 hours when the pins could not be used due to deformation by the hammer.
  Description. On September 24, 2006, station personnel were preparing the Unit 2 polar
  crane for the reactor vessel closure head removal. This involved removing the normally
  installed main hook, installing a load cell, and then reinstalling the main hook. During
  performance of Procedure OP-2504.005, Reactor Vessel Closure Head Removal,
  Revision 12, Step 7.22, licensee personnel were unable to easily remove the polar crane
  main hook pin. After the pin was removed, it was examined by the licensee and
  discovered to be mushroomed at one end. When the licensee inspected the pin used to
  secure the load cell into place, it was discovered to be in the same condition. The
  licensee determined this condition to be caused by the practice of using a hammer, as
  necessary, to both remove and install the pins during previous refueling outages.
  The inspectors noted that the licensee did not have a formal procedure that controlled
  the removal and installation of the pins, and that station personnel were controlling this
  evolution as a skill-of-the-craft process. A review of the applicable procedures by the
  inspectors revealed that Procedure OP-2504.005, Step 7.22, Reactor Vessel Closure
  Head Removal, simply states, Verify that the load cell is attached to the polar crane.
  The inspectors also determined that the use of hammers was a common practice being
  used to remove and reinstall the pins on the polar crane, and there was no existing
  evaluation for the effects of this on the integrity of the pins. The inspectors determined
  that the lack of adequate procedural direction and the practice of hammering the pins in
  and out directly contributed to the deformation of the pins. Finally, the inspectors were
  informed by licensee personnel that the practice of using hammers to remove the pins
                                            -20-                                    Enclosure
    was not part of the formal training received by maintenance personnel; however, in at
    least one instance, a discussion between instructors and maintenance personnel
    outside the formal lesson plan had occurred describing the practice of using hammers
    as being acceptable.
    Analysis. The inspectors determined that the licensees failure to provide clear guidance
    and training on how to remove the main hook and load cell pins without causing damage
    was a performance deficiency. The finding was determined to be more than minor
    because it affected the equipment performance attribute of the initiating events
    cornerstone objective to limit the likelihood of those events that upset plant stability and
    challenge critical safety functions during shutdown as well as power operations. The
    inspectors evaluated the finding using MC 0609, Significance Determination Process,
    Appendix G, Shutdown Operations Significance Determination Process. The
    inspectors determined that the finding was not a loss of shutdown control as defined by
    MC 0609, Appendix G, Table 1, and then evaluated the issue using Checklist 3 of
    MC 0609, Appendix G, Attachment 1. The inspectors determined that a quantitative
    analysis was not required because the event did not represent a reduction in mitigation
    capability which would have increased the frequency of occurrence of a loss of decay
    heat removal. Therefore, the finding was determined to have very low safety
    significance. The cause of the finding is related to the crosscutting element of human
    performance associated with resources because the training of personnel and
    procedural guidance available was adequate.
    Enforcement. While a performance deficiency was identified, there were no violations of
    NRC requirements identified during the review of this issue. The licensee has entered
    this issue into the CAP as CR ANO-2-2006-1553: Finding (FIN) 05000368/2006005-04,
    Unplanned Increase in Time with Reactor Vessel Water Level at Flange Level.
1R22 Surveillance Testing (71111.22)
  a. Inspection Scope
    The inspectors reviewed the UFSAR, procedure requirements, and TSs to ensure that
    the four below listed surveillance activities demonstrated that the SSCs tested were
    capable of performing their intended safety functions. The inspectors either witnessed
    or reviewed test data to verify that the following significant surveillance test attributes
    were adequate: (1) preconditioning; (2) evaluation of testing impact on the plant;
    (3) acceptance criteria; (4) test equipment; (5) procedures; (6) jumper/lifted lead
    controls; (7) test data; (8) testing frequency and method demonstrated TS operability;
    (9) test equipment removal; (10) restoration of plant systems; (11) fulfillment of ASME
    Code requirements; (12) updating of performance indicator (PI) data; (13) engineering
    evaluations, root causes, and bases for returning tested SSCs not meeting the test
    acceptance criteria were correct; (14) reference setting data; and (15) annunciators and
    alarms setpoints. The inspectors also verified that the licensee identified and
    implemented any needed corrective actions associated with the surveillance testing.
    *      August 4, 2006, Unit 1, makeup system Valve MU-36A local leak rate test
    *      October 5, 2006, Unit 2, main steam safety valve lifts (inservice test)
    *      October 15, 2006, Unit 2, Valve 2SV-8271-2 local leak rate test
                                              -21-                                      Enclosure
    *      October 23, 2006, Unit 2, Containment Cooler A
    Documents reviewed by the inspectors are listed in the attachment.
    The inspectors completed four samples.
  b. Findings
    No findings of significance were identified.
    Cornerstone: Emergency Preparedness
1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)
  a. Inspection Scope
    The inspector performed an in-office review of Revision 037-05-0 to Emergency Plan
    Implementing Procedure OP-1903.010, Emergency Action Level Classification. The
    revision was submitted in October 2006. The revision corrected emergency plan
    guidance for transient event classification and notification practices at Arkansas Nuclear
    One and was a corrective action for the NCV 05000313,368/2006003-02, Failure to
    Meet Immediate Notification Requirements during Transient Events.
    The revision was compared to the previous revision, to the criteria of NUREG-0654,
    Criteria for Preparation and Evaluation of Radiological Emergency Response Plans and
    Preparedness in Support of Nuclear Power Plants, Revision 1; and NEI 99-01,
    Methodology for Development of Emergency Action Levels, Revision 2; and to the
    standards in 10 CFR 50.47(b) to determine if the revision was adequately conducted
    following the requirements of 10 CFR 50.54(q). This review was not documented in a
    safety evaluation report and did not constitute approval of licensee changes, therefore,
    the revision is subject to future inspection.
    The inspector completed one sample during the inspection.
  b. Findings
    No findings of significance were identified.
1EP6 Drill Evaluation (71114.06)
  a. Inspection Scope
    For the one below listed simulator-based training evolutions contributing to drill/exercise
    performance, emergency response organization, and PIs, the inspectors: (1) observed
    the training evolution to identify any weaknesses and deficiencies in classification,
    notification, and protective action requirements (PAR) development activities;
    (2) compared the identified weaknesses and deficiencies against licensee identified
                                              -22-                                    Enclosure
      findings to determine whether the licensee is properly identifying failures;
      and (3) determined whether licensee performance is in accordance with the guidance of
      the NEI 99-02, Voluntary Submission of Performance Indicator Data, acceptance
      criteria.
      *        December 7, 2006, Unit 2, simulator-based exercise requiring notice of unusual
              event and alert declarations
      Documents reviewed by the inspectors are listed in the attachment.
      The inspectors completed one sample.
  b. Findings
      No findings of significance were identified.
2.    RADIATION SAFETY
      Cornerstone: Occupational Radiation Safety
2OS1 Access Control To Radiologically Significant Areas (71121.01)
  a. Inspection Scope
      This area was inspected to assess the licensees performance in implementing physical
      and administrative controls for airborne radioactivity areas, radiation areas, high
      radiation areas, and worker adherence to these controls. The inspectors used the
      requirements in 10 CFR Part 20, the TSs, and the licensees procedures required by
      TSs as criteria for determining compliance. During the inspection, the inspectors
      interviewed the radiation protection manager, radiation protection supervisors, and
      radiation workers. The inspectors performed independent radiation dose rate
      measurements and reviewed the following items:
      *        PI events and associated documentation packages reported by the licensee in
              the occupational radiation safety cornerstone
      *        Controls (surveys, posting, and barricades) of radiation, high radiation, or
              airborne radioactivity areas
      *        Radiation work permits, procedures, engineering controls, and air sampler
              locations
      *        Conformity of electronic personal dosimeter alarm set points with survey
              indications and plant policy; workers knowledge of required actions when their
              electronic personnel dosimeter noticeably malfunctions or alarms
      *        Barrier integrity and performance of engineering controls in airborne radioactivity
              areas
      *        Adequacy of the licensees internal dose assessment for any actual internal
              exposure greater than 50 millirem committed effective dose equivalent
                                              -23-                                      Enclosure
      *      Physical and programmatic controls for highly activated or contaminated
              materials (nonfuel) stored within spent fuel and other storage pools
      *      Self-assessments related to the access control program since the last
              inspection; there were no audits, licensee event reports, and special reports
              documented.
      *      Corrective action documents related to access controls
      *      Licensee actions in cases of repetitive deficiencies or significant individual
              deficiencies
      *      Radiation work permit briefings and worker instructions
      *      Adequacy of radiological controls such as, required surveys, radiation protection
              job coverage, and contamination controls during job performance
      *      Dosimetry placement in high radiation work areas with significant dose rate
              gradients
      *      Changes in licensee procedural controls of high dose rate - high radiation areas
              and very high radiation areas
      *      Controls for special areas that have the potential to become very high radiation
              areas during certain plant operations
      *      Posting and locking of entrances to all accessible high dose rate - high radiation
              areas and very high radiation areas
      *      Radiation worker and radiation protection technician performance with respect to
              radiation protection work requirements
      The inspectors completed 21 of the required 21 samples.
  b. Findings
      No findings of significance were identified.
4.    OTHER ACTIVITIES
4OA1 PI Verification (71151)
.1    Occupational Radiation Safety Cornerstone
  a. Inspection Scope
      The inspectors reviewed licensee documents from April through September 2006. The
      review included corrective action documentation that identified occurrences in locked high
      radiation areas (as defined in the licensees TSs, very high radiation areas (as defined in
      10 CFR 20.1003), and unplanned personnel exposures (as defined in NEI 99-02).
      Additional records reviewed included as low as reasonably achievable records and whole
      body counts of selected individual exposures. The inspectors interviewed licensee
                                              -24-                                      Enclosure


source.Enforcement.  ANO Unit 2 License Condition 2.C.(3)(b), "Fire Protection," states, in part,that the licensee shall implement and maintain all provisions of the approved fire
      personnel that were accountable for collecting and evaluating the PI data. In addition, the
protection program.  "ANO Unit 1 and Unit 2 - Fire Hazards Analysis," Revision 9, is part
      inspector toured plant areas to verify that high radiation, locked high radiation, and very
of the ANO Unit 2 fire protection program. Section 6.4.5, "Fire Barriers, Seals, and
      high radiation areas were properly controlled. PI definitions and guidance contained in
Penetrations," of the Fire Hazards Analysis states, in part, that the fire barrier system at
      NEI 99-02, Regulatory Assessment Indicator Guideline, Revision 4, were used to verify
ANO has been designed to ensure that fires will be confined or adequately retarded
      the basis in reporting for each data element.
from spreading to adjacent portions of the facility. Contrary to this, the filling to overflowof the oil collection system tank and overflow berm with water from the CCW system
      *      Occupational Exposure Control Effectiveness
-17-Enclosureduring Operating Cycle 18 prevented a potential RCP oil fire in the containmentbasement from being confined per the fire protection program. Because the finding is of
      The inspectors completed the required sample (1) in this cornerstone
very low safety significance and has been entered into the licensee's CAP as
  b. Findings
CR ANO-2-2006-1407, this violation is being treated as an NCV consistent with
      No findings of significance were identified.
Section VIA of the Enforcement Policy:  NCV 05000368/2006005-02, "Failure to Perform
.2    Public Radiation Safety Cornerstone
Modification Resulted in an Inoperable RCP Oil Collection System."1R17Permanent Plant Modifications (71111.17).1Annual ReviewThe inspectors reviewed key affected parameters associated with energy needs,materials/replacement components, timing, heat removal, control signals, equipment
  a. Inspection Scope
protection from hazards, operations, flowpaths, pressure boundary, ventilation
      The inspectors reviewed licensee documents from April through September 2006.
boundary, structural, process medium properties, licensing basis, and failure modes for
      Licensee records reviewed included corrective action documentation that identified
the modification listed below.  The inspectors verified that:  (1) modification preparation,
      occurrences for liquid or gaseous effluent releases that exceeded PI thresholds and those
staging, and implementation does not impair emergency/abnormal operating procedure
      reported to the NRC. The inspectors interviewed licensee personnel that were
actions, key safety functions, or operator response to loss of key safety functions;
      accountable for collecting and evaluating the PI data. PI definitions and guidance
(2) postmodification testing maintained the plant in a safe configuration during testing by
      contained in NEI 99-02, Regulatory Assessment Indicator Guideline, Revision 4, were
verifying that unintended system interactions will not occur, SSC performance
      used to verify the basis in reporting for each data element.
characteristics still meet the design basis, the appropriateness of modification design
      *      Radiological Effluent TS/Offsite Dose Calculation Manual Radiological Effluent
assumptions, and the modification test acceptance criteria has been met; and (3) the
              Occurrences
licensee has identified and implemented appropriate corrective actions associated with
      The inspectors completed the required sample (1) in this cornerstone
permanent plant modifications. *September 19 through October 26, 2006, Unit 2, pressurizer replacement1R19Postmaintenance Testing (71111.19)    a.Inspection ScopeThe inspectors selected the six below listed postmaintenance test activities of risksignificant systems or components. For each item, the inspectors: (1) reviewed the
  b. Findings
applicable licensing basis and/or design-basis documents to determine the safety
      No findings of significance were identified.
functions; (2) evaluated the safety functions that may have been affected by the
4OA2 Identification and Resolution of Problems (71152)
maintenance activity; and (3) reviewed the test procedure to ensure it adequately tested
.1    Routine Review of Identification and Resolution of Problems
the safety function that may have been affected.  The inspectors either witnessed or
      The inspectors performed a daily screening of items entered into the licensees CAP.
reviewed test data to verify that acceptance criteria were met, plant impacts were
      This assessment was accomplished by reviewing CRs and attending corrective action
evaluated, test equipment was calibrated, procedures were followed, jumpers were
      review and work control meetings. The inspectors: (1) verified that equipment, human
properly controlled, the test data results were complete and accurate, the test
      performance, and program issues were being identified by the licensee at an appropriate
equipment was removed, the system was properly realigned, and deficiencies during
      threshold and that the issues were entered into the CAP; (2) verified that corrective
testing were documented.  The inspectors also reviewed the UFSAR to determine if the
      actions were commensurate with the significance of the issue; and (3) identified conditions
licensee identified and corrected problems related to postmaintenance testing.*October 17, 2006, Unit 1, Emergency Feedwater Pump P-7A
      that might warrant additional follow-up through other baseline inspection procedures.
*October 22, 2006, Unit 2, pressurizer heater capacity
.2    Selected Issue Follow-up Inspection
*October 24, 2006, Unit 2, replacement pressurizer relief valve monitor test 
      In addition to the routine review, the inspectors selected the two below listed issues for a
-18-Enclosure*October 25, 2006, Unit 2, containment spray header repairs *October 27, 2006, Unit 2, replacement pressurizer leakage
      more in-depth review. The inspectors considered the following during the review of the
*November 1, 2006, Unit 2, containment building personnel hatch leakage rate
      licensees actions: (1) complete and accurate identification of the problem in a timely
testingDocuments reviewed by the inspectors are listed in the attachment.
                                                -25-                                     Enclosure
The inspectors completed six samples.    b.FindingsNo findings of significance were identified.1R20Refueling and Outage Activities (71111.20)1.Unit 2 Forced Outage Caused by Fire in Motor Control Center 2B-53    a.Inspection ScopeThe inspectors reviewed the following risk significant outage activities to verify defensein depth commensurate with the outage risk control plan and compliance with the TSs:
 
(1) the risk control plan, (2) tagging/clearance activities,  (3) heatup and cooldown
      manner; (2) evaluation and disposition of operability/reportability issues; (3) consideration
activities, and (4) restart activities. The inspectors completed one sample.    b.FindingsNo findings of significance were identified.2.Refueling and Pressurizer Replacement Outage 2R18    a.Inspection ScopeThe inspectors reviewed the following risk significant refueling items or outage activitiesto verify defense in depth commensurate with the outage risk control plan, compliance
      of extent of condition, generic implications, common cause, and previous occurrences;
with the TSs, and adherence to commitments in response to Generic Letter 88-17, "Loss
      (4) classification and prioritization of the resolution of the problem; (5) identification of root
of Decay Heat Removal":  (1) the risk control plan, (2) tagging/clearance activities,
      and contributing causes of the problem; (6) identification of corrective actions;
(3) RCS instrumentation, (4) electrical power, (5) decay heat removal, (6) spent fuel pool
      and (7) completion of corrective actions in a timely manner.
cooling, (7) inventory control, (8) reactivity control, (9) containment closure, (10) reduced
      *       September 20, 2006, Unit 2, repeat occurrence of containment purge isolation
inventory conditions, (11) refueling activities, (12) heatup and cooldown activities,
      *       October 30, 2006, Unit 2, repeat occurrence of improper electrical connections in
(13) restart activities, and (14) licensee identification and implementation of appropriate
              motor-control centers
corrective actions associated with refueling and outage activities.  The inspectors'
      When evaluating the effectiveness of the licensees corrective actions for these issues,
containment inspections included observation of the containment sump for damage and
      the following attributes were considered:
debris, supports, braces, and snubbers for evidence of excessive stress, water hammer,
      *       Complete and accurate identification of the problem in a timely manner
or aging.  
              commensurate with its significance and ease of discovery
-19-EnclosureThe inspectors completed one sample.    b.Findings.1Inadvertent RCS Draining While in Mode 5Introduction.  A Green self-revealing noncited violation of the licensee's TS requirementfor procedures was identified when an operator failed to close a resin sluice header
      *       Evaluation and disposition of operability and reportability issues
drain valve as required by procedure.  Later, while operators were aligning the unit for
      *        Consideration of extent of condition, generic implications, common cause, and
alternate reactor coolant purification, a loss of approximately 230 gallons of RCS
              previous occurrences
inventory occurred. Description.  On September 14, 2006, operations personnel performedProcedure OP-2104.019, "Clean Resin Transfer," to add clean resin to Purification Ion
      *        Classification and prioritization of the resolution of the problem commensurate with
Exchanger 2T-36B.  During this procedure, Valve 2DCH-11 was opened as part of the
              its safety significance
system lineup.  Subsequently, when the evolution was completed and the plant lineup
      *        Identification of root and contributing causes of the problem for significant
was being restored, station personnel failed to properly perform Step 22.2 of the
              conditions adverse to quality
procedure leaving Valve 2DCH-11 in the open position.  Subsequently, on September 21, 2006, with Unit 2 in Mode 5, the licensee was in theprocess of aligning alternate purification in accordance with Procedure OP-2104.004,
      *        Identification of corrective actions which are appropriately focused to correct the
"Shutdown Cooling System," Attachment J, "Alternate Purification."  When Step 2.11 of
              problem
this procedure was performed, the control room operators noted that pressurizer level
      *        Completion of corrective actions in a timely manner commensurate with the safety
began to lower.  The evolution was stopped and the lineup was secured. At this point,
              significance of the issue
pressurizer level stopped lowering.  Station personnel performed a system walkdown
      Documents reviewed by the inspectors are listed in the attachment
and discovered that Valve 2DCH-11 was in the open position.  Operations personnel
.3   Semiannual Trend Review
determined that approximately 230 gallons were drained from the RCS through the open
  a. Inspection Scope
valve.During their review, the inspectors noted that Procedure OP-2104.004, Attachment J,directed personnel to prepare a caution tag for components to prevent the loss of RCS
      The inspectors completed a semi-annual trend review of repetitive or closely related
inventory.  However, the procedure contained a note that preceded Step 1.11 which
      issues that were documented in corrective action documents to identify trends that might
directed the caution tag be hung on the room door instead of Valve 2DCH-11 and two
      indicate the existence of more safety-significant issues. The inspectors' review consisted
other valves. This tag stated that, since the valves were normally closed, any
      of the 6-month period of June 24 through December 31, 2006. When warranted, some of
misalignment would be detected by system abnormalities. The inspectors determined
      the samples expanded beyond those dates to fully assess the issue. The inspectors also
that this note contributed to Valve 2DCH-11 not being discovered out of position prior to
      reviewed CAP items associated with deficiencies in the conduct of activities involving hot
initiating alternate purification since the licensee did not perform a valve lineup
      work. The inspectors compared and contrasted their results with the results contained in
verification.Analysis.  The failure of station personnel to manipulate Valve 2DCH-11 in accordancewith station procedure was determined to be a performance deficiency. The finding was
      the licensees quarterly trend reports. Corrective actions associated with a sample of the
determined to be more than minor because it affected the configuration control attribute
      issues identified in the licensees trend report were reviewed for adequacy. Documents
of the initiating events cornerstone objective to limit the likelihood of those events that
      reviewed by the inspectors are listed in the attachment.
upset plant stability and challenge critical safety functions during shutdown as well as
                                                  -26-                                     Enclosure
power operations. The inspectors used MC 0609, "Significance Determination Process,"
 
Appendix G, "Shutdown Operations Significance Determination Process," and assumed
  b. Findings
that the administrative controls implemented to avoid operations that could lead to
      During the Unit 2 pressurizer replacement Refueling Outage 2R18 from September 19
perturbations in RCS level control attribute was affected. The finding was determined to
      through October 28, 2006, several deficiencies were noted involving the conduct of hot
have very low safety significance because the finding did not result in a loss of 2 feet or
      work. Licensee Procedure EN-DC-127, Control of Hot Work and Ignition Sources,
-20-Enclosuremore of RCS inventory and did not result in a loss of RCS inventory while the unit was inreduced inventory. The cause of the finding is related to the crosscutting aspect ofhuman performance associated with work practices because the operator failed to use
      contains the governing guidelines for the conduct of hot work, including Hot Work
error prevention techniques like self checking and peer checking which would have
      Permit, Attachment 8.1, which serves to document that the applicable requirements for
prevented the event.Enforcement.  Unit 2 TS, Section 6.4.1.a, "Procedures," requires, in part, that writtenprocedures shall be established, implemented, and maintained covering the applicable
      each activity involving hot work are met. Examples of instances resulting from failures to
procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A,
      adequately implement the control of hot work procedure included:
February 1978.  Procedure OP-2104.019, "Clean Resin Transfer," is a procedure
      *      On September 24, 2006, welding activities being conducted on the Unit 2 main
required by Regulatory Guide 1.33.  Contrary to the above, on September 14, 2006, the
              condenser manway cover resulted in paint/crud smoldering that was extinguished
licensee failed to fully implement Procedure OP-2104.019, "Clean Resin Transfer,"
              with a portable fire extinguisher.
when the licensee failed to close Valve 2DCH-11. Because this finding is of very low
      *      On September 25, 2006, sparks from torch cutting of the Unit 2 containment sump
safety significance and has been entered into the CAP as CR ANO-2-2006-1464, this
              strainer ignited a nearby plastic bag containing used anti-contamination clothing.
violation is being treated as an NCV, consistent with Section VIA of the NRC
      *      On September 26, 2006, a substantial amount of slag from the containment sump
Enforcement Policy:  NCV 05000368/2006005-03, "Inadvertent RCS Draining While in
              strainer torch cutting flowed down onto a fire blanket that was protecting the floor
Mode 5.".2Unplanned Increase in Time with Reactor Vessel Water Level at Flange LevelIntroduction.  A Green self-revealing finding was identified associated with the licensee'suse of a hammer to remove and reinstall both the main hook pin and the load cell pin on
              and caused the fire blanket to ignite.
the Unit 2 polar crane. Unit 2 was maintained in a condition with reactor vessel water
      *      On September 27, 2006, slag from the containment sump strainer torch cutting
level being maintained just below the reactor vessel flange for an additional unplanned
              flowed down through a fire blanket and landed on Valve 2BS-38 in the containment
27 hours when the pins could not be used due to deformation by the hammer. Description. On September 24, 2006, station personnel were preparing the Unit 2 polarcrane for the reactor vessel closure head removal.  This involved removing the normally
              sump. The slag came in contact with debris buildup on the valve locking chain and
installed main hook, installing a load cell, and then reinstalling the main hook.  During
              began to smoke and smolder. A portable fire extinguisher was discharged to
performance of Procedure OP-2504.005, "Reactor Vessel Closure Head Removal,"
              extinguish the smoldering.
Revision 12, Step 7.22, licensee personnel were unable to easily remove the polar crane
      *      On September 28, 2006, the firewatch posted for the containment sump strainer
main hook pin.  After the pin was removed, it was examined by the licensee and
              hot work could not get to his designated fire extinguisher. The firewatch had
discovered to be mushroomed at one end. When the licensee inspected the pin used to
              moved to the east side of the sump and the extinguisher remained on the west
secure the load cell into place, it was discovered to be in the same condition.  The
              side of the sump.
licensee determined this condition to be caused by the practice of using a hammer, as
      *      On October 5, 2006, a small fire in the Unit 2 containment building basement
necessary, to both remove and install the pins during previous refueling outages. The inspectors noted that the licensee did not have a formal procedure that controlledthe removal and installation of the pins, and that station personnel were controlling this
              below the pressurizer was extinguished by the assigned firewatch using a portable
evolution as a skill-of-the-craft process.  A review of the applicable procedures by the
              extinguisher.
inspectors revealed that Procedure OP-2504.005, Step 7.22, "Reactor Vessel Closure
      *      On October 16, 2006, welding and grinding activities above the replacement
Head Removal," simply states, "Verify that the load cell is attached to the polar crane."
              pressurizer were being performed without proper protection to prevent sparks from
The inspectors also determined that the use of hammers was a common practice being
              traveling down the cavity below.
used to remove and reinstall the pins on the polar crane, and there was no existing
      The licensee entered each of these occurrences into their CAP.
evaluation for the effects of this on the integrity of the pins. The inspectors determined
.4    Access Control to Radiologically Significant Areas
that the lack of adequate procedural direction and the practice of hammering the pins in
      Section 2OS1 evaluated the effectiveness of the licensee's problem identification and
and out directly contributed to the deformation of the pins. Finally, the inspectors were
      resolution processes regarding access controls to radiologically significant areas and
informed by licensee personnel that the practice of using hammers to remove the pins
      radiation worker practices. The inspectors reviewed corrective action documents for root
-21-Enclosurewas not part of the formal training received by maintenance personnel; however, in atleast one instance, a discussion between instructors and maintenance personnel
      cause/apparent cause analysis against the licensees problem identification and resolution
outside the formal lesson plan had occurred describing the practice of using hammers
      process. No findings of significance were identified.
as being acceptable.Analysis.  The inspectors determined that the licensee's failure to provide clear guidanceand training on how to remove the main hook and load cell pins without causing damage
                                                -27-                                  Enclosure
was a performance deficiency. The finding was determined to be more than minor
 
because it affected the equipment performance attribute of the initiating events
4OA3 Follow-up of Events and Notices of Enforcement Discretion (71153)
cornerstone objective to limit the likelihood of those events that upset plant stability and
  a. Inspection Scope
challenge critical safety functions during shutdown as well as power operations.  The
    The inspectors: (1) reviewed operator logs, plant computer data, and/or strip charts for
inspectors evaluated the finding using MC 0609, "Significance Determination Process,"
    the below listed evolutions to evaluate operator performance in coping with nonroutine
Appendix G, "Shutdown Operations Significance Determination Process."  The
    events and transients; (2) verified that operator actions were in accordance with the
inspectors determined that the finding was not a loss of shutdown control as defined by
    response required by plant procedures and training; and (3) verified that the licensee has
MC 0609, Appendix G, Table 1, and then evaluated the issue using Checklist 3 of
    identified and implemented appropriate corrective actions associated with personnel
MC 0609, Appendix G, Attachment 1.  The inspectors determined that a quantitative
    performance problems that occurred during the nonroutine evolutions sampled.
analysis was not required because the event did not represent a reduction in mitigation
    *        October 26, 2006, Unit 1, fish intrusion into the circulating water system
capability which would have increased the frequency of occurrence of a loss of decay
    *        October 30, 2006, Unit 2, fire in Motor-Control Center 2B-53
heat removal. Therefore, the finding was determined to have very low safety
    *        November 9, 2006, Unit 1, unplanned loss of Main Feedwater Pump P-2A
significance.  The cause of the finding is
    Documents reviewed by the inspectors are listed in the attachment.
related to the crosscutting element of humanperformance associated with resources because the training of personnel and
    The inspectors completed three samples.
procedural guidance available was adequate.Enforcement.  While a performance deficiency was identified, there were no violations ofNRC requirements identified during the review of this issue.  The licensee has entered
  b. Findings
this issue into the CAP as CR ANO-2-2006-1553:  Finding (FIN) 05000368/2006005-04,
    Introduction. A Green self-revealing finding was identified when the licensee replaced an
"Unplanned Increase in Time with Reactor Vessel Water Level at Flange Level."1R22Surveillance Testing  (71111.22)    a.Inspection ScopeThe inspectors reviewed the UFSAR, procedure requirements, and TSs to ensure thatthe four below listed surveillance activities demonstrated that the SSCs tested were
    air conditioning unit for the Unit 1 Main Feedwater Pump (MFP) A control cabinet without
capable of performing their intended safety functions. The inspectors either witnessed
    considering the effects of electromagnetic interference (EMI) on the digital speed
or reviewed test data to verify that the following significant surveillance test attributes
    monitor (DSM) housed in the cabinet. Consequently, MFP A tripped, resulting in an
were adequate:  (1) preconditioning; (2) evaluation of testing impact on the plant;
    unplanned automatic plant power reduction from 100 percent to 40 percent RTP.
(3) acceptance criteria; (4) test equipment; (5) procedures; (6) jumper/lifted lead
    Description. In September 2006 the air conditioning unit for the Unit 1 MFP A cabinet
controls; (7) test data; (8) testing frequency and method demonstrated TS operability;
    failed. During the procurement phase of replacement efforts, the station discovered that
(9) test equipment removal; (10) restoration of plant systems; (11) fulfillment of ASME
    the current air conditioning unit was no longer available because it had become obsolete.
Code requirements; (12) updating of performance indicator (PI) data; (13) engineering
    The licensee contacted the cabinet manufacturer who recommended to the licensee a
evaluations, root causes, and bases for returning tested SSCs not meeting the test
    replacement unit. On October 12 the licensee replaced the air conditioning unit with the
acceptance criteria were correct; (14) reference setting data; and (15) annunciators and
    recommended replacement after evaluating it as being an equivalent unit in accordance
alarms setpoints. The inspectors also verified that the licensee identified and
    with Procedure EN-DC-313, Procurement Engineering Process, Revision 0.
implemented any needed corrective actions associated with the surveillance testing. *August 4, 2006, Unit 1, makeup system Valve MU-36A local leak rate test*October 5, 2006, Unit 2, main steam safety valve lifts (inservice test)
    Subsequently, on November 9, 2006, while Unit 1 was operating at 100 percent RTP
*October 15, 2006, Unit 2, Valve 2SV-8271-2 local leak rate test
    MFP A tripped, which caused the integrated control system to initiate and perform an
-22-Enclosure*October 23, 2006, Unit 2, Containment Cooler ADocuments reviewed by the inspectors are listed in the attachment.
    unplanned automatic power reduction to 40 percent RTP. Operators surveyed the
The inspectors completed four samples.    b.FindingsNo findings of significance were identified.
    indications and concluded that the cause of the MFP trip was an overspeed condition;
Cornerstone:  Emergency Preparedness1EP4Emergency Action Level and Emergency Plan Changes (71114.04)    a.Inspection ScopeThe inspector performed an in-office review of Revision 037-05-0 to Emergency PlanImplementing Procedure OP-1903.010, "Emergency Action Level Classification."  The
    however, at the time of the trip, there were no indications that the MFP had actually
revision was submitted in October 2006.  The revision corrected emergency plan
    experienced an overspeed.
guidance for transient event classification and notification practices at Arkansas Nuclear
    After extensive troubleshooting, the licensee suspected that EMI from the air conditioning
One and was a corrective action for the NCV 05000313,368/2006003-02, "Failure to
    unit was the cause of the faults. The licensee performed a review of the new air
Meet Immediate Notification Requirements during Transient Events."The revision was compared to the previous revision, to the criteria of NUREG-0654, "Criteria for Preparation and Evaluation of Radiological Emergency Response Plans and
    conditioning unit and identified that the bottom section of the new unit was molded plastic
Preparedness in Support of Nuclear Power Plants," Revision 1; and NEI 99-01,
    and not metal like the previous unit. They also discovered the configuration of this new
"Methodology for Development of Emergency Action Levels," Revision 2; and to the
    unit placed the blower fan directly above, and in closer proximity to, the DSM than did that
standards in 10 CFR 50.47(b) to determine if the revision was adequately conducted
    of the previous air conditioning unit. The licensee decided to remove power to the air
following the requirements of 10 CFR 50.54(q).  This review was not documented in a
    conditioning unit to verify that it was the initiator of the faults in the DSM. With power to
safety evaluation report and did not constitute approval of licensee changes, therefore,
    the air conditioning unit removed, the faults and trips did not recur.
the revision is subject to future inspection.The inspector completed one sample during the inspection.     b.FindingsNo findings of significance were identified.1EP6Drill Evaluation (71114.06)    a.Inspection ScopeFor the one below listed simulator-based training evolutions contributing to drill/exerciseperformance, emergency response organization, and PIs, the inspectors:  (1) observed
                                                -28-                                     Enclosure
the training evolution to identify any weaknesses and deficiencies in classification,notification, and protective action requirements (PAR) development activities;
 
(2) compared the identified weaknesses and deficiencies against licensee identified
      The inspectors reviewed the licensees root cause evaluation of this event, documented in
-23-Enclosurefindings to determine whether the licensee is properly identifying failures;and (3) determined whether licensee performance is in accordance with the guidance of
      CR ANO-1-2006-1399, which determined the root cause to be that the procurement
the NEI 99-02, "Voluntary Submission of Performance Indicator Data," acceptance
      engineering equivalency guidelines did not consider EMI as a potential failure mode.
criteria.*December 7, 2006, Unit 2, simulator-based exercise requiring notice of unusualevent and alert declarationsDocuments reviewed by the inspectors are listed in the attachment.  
      During this review, the inspectors noted that the licensee had not questioned or
The inspectors completed one sample.     b.FindingsNo findings of significance were identified.2.RADIATION SAFETYCornerstone:  Occupational Radiation Safety2OS1Access Control To Radiologically Significant Areas (71121.01)    a.Inspection ScopeThis area was inspected to assess the licensee's performance in implementing physicaland administrative controls for airborne radioactivity areas, radiation areas, high
      investigated any of the differences between the old and the new air conditioning units.
radiation areas, and worker adherence to these controls.  The inspectors used the
      Instead, the licensee had relied on the manufacturers designation that the new unit was
requirements in 10 CFR Part 20, the TSs, and the licensee's procedures required by
      an equivalent replacement for the old unit.
TSs as criteria for determining compliance.  During the inspection, the inspectors
      Also, during their review of the root cause analysis, the inspectors noted that there had
interviewed the radiation protection manager, radiation protection supervisors, and
      been previous experiences with the MFP A control system involving EMI, as well as a
radiation workers. The inspectors performed independent radiation dose rate
      substantial amount of industry operating experience concerning the topic of EMI and
measurements and reviewed the following items:*PI events and associated documentation packages reported by the licensee inthe occupational radiation safety cornerstone *Controls (surveys, posting, and barricades) of radiation, high radiation, orairborne radioactivity areas*Radiation work permits, procedures, engineering controls, and air samplerlocations*Conformity of electronic personal dosimeter alarm set points with surveyindications and plant policy; workers' knowledge of required actions when their
      digital components. During interviews with station personnel, the inspectors also
electronic personnel dosimeter noticeably malfunctions or alarms*Barrier integrity and performance of engineering controls in airborne radioactivityareas*Adequacy of the licensee's internal dose assessment for any actual internalexposure greater than 50 millirem committed effective dose equivalent
      determined that station engineers received specific training on EMI related to digital
-24-Enclosure*Physical and programmatic controls for highly activated or contaminatedmaterials (nonfuel) stored within spent fuel and other storage pools*Self-assessments related to the access control program since the lastinspection; there were no audits, licensee event reports, and special reports
      components.
documented.*Corrective action documents related to access controls
      Analysis. The inspectors determined that the failure of the licensee to adequately
*Licensee actions in cases of repetitive deficiencies or significant individualdeficiencies*Radiation work permit briefings and worker instructions
      evaluate the new air conditioning unit with respect to design differences and possible
*Adequacy of radiological controls such as, required surveys, radiation protectionjob coverage, and contamination controls during job performance *Dosimetry placement in high radiation work areas with significant dose rategradients*Changes in licensee procedural controls of high dose rate - high radiation areasand very high radiation areas*Controls for special areas that have the potential to become very high radiationareas during certain plant operations*Posting and locking of entrances to all accessible high dose rate - high radiationareas and very high radiation areas *Radiation worker and radiation protection technician performance with respect toradiation protection work requirements The inspectors completed 21 of the required 21 samples.      b.FindingsNo findings of significance were identified.4.OTHER ACTIVITIES
      EMI interactions was a performance deficiency. The finding was determined to be more
4OA1PI Verification (71151).1Occupational Radiation Safety Cornerstone    a.Inspection ScopeThe inspectors reviewed licensee documents from April through September 2006. Thereview included corrective action documentation that identified occurrences in locked high
      than minor because it affected the design control attribute of the initiating events
radiation areas (as defined in the licensee's TSs, very high radiation areas (as defined in10 CFR 20.1003), and unplanned personnel exposures (as defined in NEI 99-02).
      cornerstone objective to limit the likelihood of those events that upset plant stability and
Additional records reviewed included as low as reasonably achievable records and wholebody counts of selected individual exposures.  The inspectors interviewed licensee
      challenge critical safety functions during shutdown as well as power operations. Using the
-25-Enclosurepersonnel that were accountable for collecting and evaluating the PI data.  In addition, theinspector toured plant areas to verify that high radiation, locked high radiation, and very
      MC 0609, Significance Determination Process, Phase 1 Worksheet, the finding is
high radiation areas were properly controlled.
      determined to have very low safety significance because the condition only affected the
  PI definitions and guidance contained inNEI 99-02, "Regulatory Assessment Indicator Guideline," Revision 4, were used to verify
      initiating events cornerstone and did not contribute to both the likelihood of a reactor trip
the basis in reporting for each data element.*Occupational Exposure Control Effectiveness
      and the likelihood that mitigation equipment or functions will not be available. The cause
The inspectors completed the required sample (1) in this cornerstone    b.FindingsNo findings of significance were identified..2Public Radiation Safety Cornerstone    a.Inspection ScopeThe inspectors reviewed licensee documents from April through September 2006. Licensee records reviewed included corrective action documentation that identified
      of the finding is related to the crosscutting element of problem identification and resolution
occurrences for liquid or gaseous effluent releases that exceeded PI thresholds and those
      associated with operating experience because the licensees failure to implement and
reported to the NRC. The inspectors interviewed licensee personnel that were
      institutionalize OE through changes to station processes and procedures.
accountable for collecting and evaluating the PI data. PI definitions and guidance
      Enforcement. While a performance deficiency was identified with regard to the trip of the
contained in NEI 99-02, "Regulatory Assessment Indicator Guideline," Revision 4, were
      MFP A, there were no violations identified during the review of this issue. The licensee
used to verify the basis in reporting for each data element.*Radiological Effluent TS/Offsite Dose Calculation Manual  Radiological EffluentOccurrencesThe inspectors completed the required sample (1) in this cornerstone    b.FindingsNo findings of significance were identified.4OA2Identification and Resolution of Problems (71152).1Routine Review of Identification and Resolution of ProblemsThe inspectors performed a daily screening of items entered into the licensee's CAP. This assessment was accomplished by reviewing CRs and attending corrective action
      has entered this issue into the CAP as CR ANO-1-2006-1399: FIN 05000313/2006005-5,
review and work control meetings. The inspectors:  (1) verified that equipment, human
      Trip of a MFP Due to Inadequate Design Control.
performance, and program issues were being identified by the licensee at an appropriate
4OA5 Other Activities
threshold and that the issues were entered into the CAP; (2) verified that corrective
.1    (Closed) Temporary Instruction (TI) 2515/169, Mitigating Systems Performance
actions were commensurate with the significance of the issue; and (3) identified conditions
      Index (MSPI) Verification
that might warrant additional follow-up through other baseline inspection procedures..2Selected Issue Follow-up InspectionIn addition to the routine review, the inspectors selected the two below listed issues for amore in-depth review. The inspectors considered the following during the review of the
  a. Inspection Scope
licensee's actions: (1)  complete and accurate identification of the problem in a timely
      During this inspection period, the inspectors completed a review of the licensees
-26-Enclosuremanner; (2) evaluation and disposition of operability/reportability issues; (3) considerationof extent of condition, generic implications, common cause, and previous occurrences;
      implementation of the MSPI in accordance with the guidance provided in TI 2515/169.
(4) classification and prioritization of the resolution of the problem; (5) identification of root
      The review examined the licensees MSPI Basis Documents (ANO1-A-6-0001, Revision 1,
and contributing causes of the problem; (6) identification of corrective actions;
      and ANO2-SA-06-00001, Revision 0) and verified the established system boundaries and
and (7) completion of corrective actions in a timely manner.*September 20, 2006, Unit 2, repeat occurrence of containment purge isolation
      monitored components were consistent with guidance provided in NEI 99-02, Reactor
*October 30, 2006, Unit 2, repeat occurrence of improper electrical connections inmotor-control centersWhen evaluating the effectiveness of the licensee's corrective actions for these issues,the following attributes were considered:*Complete and accurate identification of the problem in a timely mannercommensurate with its significance and ease of discovery*Evaluation and disposition of operability and reportability issues
      Oversight Process Performance Indicators, Revision 4. The inspectors verified that the
*Consideration of extent of condition, generic implications, common cause, andprevious occurrences*Classification and prioritization of the resolution of the problem commensurate withits safety significance*Identification of root and contributing causes of the problem for significantconditions adverse to quality*Identification of corrective actions which are appropriately focused to correct theproblem*Completion of corrective actions in a timely manner commensurate with the safetysignificance of the issueDocuments reviewed by the inspectors are listed in the attachment.3Semiannual Trend Review    a.Inspection ScopeThe inspectors completed a semi-annual trend review of repetitive or closely relatedissues that were documented in corrective action documents to identify trends that might
      licensee did not include credit for unavailability hours for short term unavailability or
indicate the existence of more safety-significant issues.  The inspectors' review consisted
      operator recovery actions to restore the risk-significant function as is allowed by
of the 6-month period of June 24 through December 31, 2006.  When warranted, some of
      NEI 99-02.
the samples expanded beyond those dates to fully assess the issue.  The inspectors also
                                                -29-                                   Enclosure
reviewed CAP items associated with deficiencies in the conduct of activities involving hot
 
work.  The inspectors compared and contrasted their results with the results contained in
      Additionally, the inspectors reviewed the baseline MSPI unavailability time using plant
the licensee's quarterly trend reports.  Corrective actions associated with a sample of the
      specific values for the period of 2002 through 2004. The verification included all planned
issues identified in the licensee's trend report were reviewed for adequacy.  Documents
      and unplanned unavailability. For Unit 1, the inspectors reviewed the baseline MSPI
reviewed by the inspectors are listed in the attachment.
      unreliability data using plant specific values for the period of 2002 through 2004. Unit 2
-27-Enclosure    b.FindingsDuring the Unit 2 pressurizer replacement Refueling Outage 2R18 from September 19through October 28, 2006, several deficiencies were noted involving the conduct of hot
      derived its baseline unreliability on industry standard values, as is permitted by NEI 99-02.
work.  Licensee Procedure EN-DC-127, "Control of Hot Work and Ignition Sources,"
      The plant specific data for 2005 through 2006 were also reviewed to ensure the licensee
contains the governing guidelines for the conduct of hot work, including "Hot Work
      properly accounted for the actual unavailability hours of MSPI systems. For the same
Permit," Attachment 8.1, which serves to document that the applicable requirements for
      period, the MSPI component unreliability data was examined to ensure the licensee
each activity involving hot work are met.  Examples of instances resulting from failures to
      identified all failures of monitored components. The accuracy and completeness of the
adequately implement the control of hot work procedure included:*On September 24, 2006, welding activities being conducted on the Unit 2 maincondenser manway cover resulted in paint/crud smoldering that was extinguished
      reported unavailability and unreliability data was verified by reviewing operating logs, CRs,
with a portable fire extinguisher.*On September 25, 2006, sparks from torch cutting of the Unit 2 containment sumpstrainer ignited a nearby plastic bag containing used anti-contamination clothing.  *On September 26, 2006, a substantial amount of slag from the containment sumpstrainer torch cutting flowed down onto a fire blanket that was protecting the floor
      and work order documents. The unavailability and unreliability data was compared with PI
and caused the fire blanket to ignite.*On September 27, 2006, slag from the containment sump strainer torch cuttingflowed down through a fire blanket and landed on Valve 2BS-38 in the containment
      data submitted to the NRC to ensure that any discrepancies would not result in a change
sump.  The slag came in contact with debris buildup on the valve locking chain and
      to the index color.
began to smoke and smolder.  A portable fire extinguisher was discharged to
  b. Findings
extinguish the smoldering.*On September 28, 2006, the firewatch posted for the containment sump strainerhot work could not get to his designated fire extinguisher.  The firewatch had
      No findings of significance were identified. This completes the inspection requirements
moved to the east side of the sump and the extinguisher remained on the west
      for this TI.
side of the sump. *On October 5, 2006, a small fire in the Unit 2 containment building basementbelow the pressurizer was extinguished by the assigned firewatch using a portable
.2    Institute of Nuclear Power Operations Plant Assessment Report Review
extinguisher.*On October 16, 2006, welding and grinding activities above the replacementpressurizer were being performed without proper protection to prevent sparks from
  a. Inspection Scope
traveling down the cavity below. The licensee entered each of these occurrences into their CAP..4Access Control to Radiologically Significant AreasSection 2OS1 evaluated the effectiveness of the licensee's problem identification andresolution processes regarding access controls to radiologically significant areas and
      The inspectors reviewed the final report for the Institute of Nuclear Power Operations
radiation worker practices.  The inspectors reviewed corrective action documents for root
      plant assessment of Arkansas Nuclear One, Units 1 and 2, conducted in July and
cause/apparent cause analysis against the licensee's problem identification and resolution
      August 2006. The inspectors reviewed the report to ensure that issues identified were
process.  No findings of significance were identified.
      consistent with the NRC perspectives of licensee performance and to verify if any
-28-Enclosure4OA3Follow-up of Events and Notices of Enforcement Discretion (71153)    a.Inspection ScopeThe inspectors:  (1) reviewed operator logs, plant computer data, and/or strip charts forthe below listed evolutions to evaluate operator performance in coping with nonroutine
      significant safety issues were identified that required further NRC followup.
events and transients; (2) verified that operator actions were in accordance with the
  b. Findings
response required by plant procedures and training; and (3) verified that the licensee has
      No findings of significance were identified.
identified and implemented appropriate corrective actions associated with personnel
.3    (Closed) Unresolved Item (URI) 05000313/2006003-01, Failure to Retrieve Required
performance problems that occurred during the nonroutine evolutions sampled. *October 26, 2006, Unit 1, fish intrusion into the circulating water system*October 30, 2006, Unit 2, fire in Motor-Control Center 2B-53
      Records of Activities Affecting Quality
*November 9, 2006, Unit 1, unplanned loss of Main Feedwater Pump P-2ADocuments reviewed by the inspectors are listed in the attachment.
      In response to inspectors questioning the seismic capability of the Tendon Surveillance
The inspectors completed three samples.      b.FindingsIntroduction.  A Green self-revealing finding was identified when the licensee replaced anair conditioning unit for the Unit 1 Main Feedwater Pump (MFP) A control cabinet without
      Cranes L-28 on Unit 1, the licensee could not locate the appropriate documentation. The
considering the effects of electromagnetic interference (EMI) on the digital speed
      licensee evaluated the as found conditions of the cranes against the uniformed building
monitor (DSM) housed in the cabinet.  Consequently, MFP A tripped, resulting in an
      code. The licensee concluded that the cranes would be able to withstand the design
unplanned automatic plant power reduction from 100 percent to 40 percent RTP.Description.  In September 2006 the air conditioning unit for the Unit 1 MFP A cabinetfailed.  During the procurement phase of replacement efforts, the station discovered that
      basis earthquake without affecting mitigating equipment. These evaluations were
the current air conditioning unit was no longer available because it had become obsolete. The licensee contacted the cabinet manufacturer who recommended to the licensee a
      reviewed by the inspectors. No findings of significance were identified, and no violations
replacement unit.  On October 12 the licensee replaced the air conditioning unit with the
      of NRC requirements were identified. The licensee documented the evaluations
recommended replacement after evaluating it as being an equivalent unit in accordance
      demonstrating the seismic qualification in CR ANO-1-2005-3109. This unresolved
with Procedure EN-DC-313, "Procurement Engineering Process," Revision 0. Subsequently, on November 9, 2006, while Unit 1 was operating at 100 percent RTPMFP A tripped, which caused the integrated control system to initiate and perform an
      item (URI) is closed.
unplanned automatic power reduction to 40 percent RTP.  Operators surveyed the
                                                -30-                                  Enclosure
indications and concluded that the cause of the MFP trip was an overspeed condition;
 
however, at the time of the trip, there were no indications that the MFP had actually
.4  NRC TI 2515/166, PWR Containment Sump Blockage
experienced an overspeed. After extensive troubleshooting, the licensee suspected that EMI from the air conditioningunit was the cause of the faults.  The licensee performed a review of the new air
    The inspectors reviewed ANOs Unit 2 implementation of plant modifications and
conditioning unit and identified that the bottom section of the new unit was molded plasticand not metal like the previous unit.  They also discovered the configuration of this new
    procedure changes committed to in their response to Generic Letter 2004-02, Potential
unit placed the blower fan directly above, and in closer proximity to, the DSM than did that
    Impact of Debris on Emergency Recirculation During Design Basis Accidents at
of the previous air conditioning unit.  The licensee decided to remove power to the air
    Pressurized Water Reactors.
conditioning unit to verify that it was the initiator of the faults in the DSM.  With power to
    The inspectors observed installation of the containment recirculation sump strainers,
the air conditioning unit removed, the faults and trips did not recur. 
    debris barriers, and interceptors. In addition, the inspectors verified that ANO Unit 2 has
-29-EnclosureThe inspectors reviewed the licensee's root cause evaluation of this event, documented inCR ANO-1-2006-1399, which determined the root cause to be that the procurement
    implemented specific procedure changes to control tags, labels, tape, and other objects
engineering equivalency guidelines did not consider EMI as a potential failure mode.
    inside the containment building.
During this review, the inspectors noted that the licensee had not questioned or
    At the time of the inspection, industry testing for chemical effects on containment
investigated any of the differences between the old and the new air conditioning units.
    recirculation sumps was not complete. Since the testing was not complete, ANO Unit 2
Instead, the licensee had relied on the manufacturer's designation that the new unit was
    evaluated the new recirculation sump modifications to the original design basis,
an equivalent replacement for the old unit.Also, during their review of the root cause analysis, the inspectors noted that there hadbeen previous experiences with the MFP A control system involving EMI, as well as a
    Regulatory Guide 1.82, Water Sources for Long-Term Recirculation Cooling Following a
substantial amount of industry operating experience concerning the topic of EMI and
    Loss-of-Coolant Accident, Revision 0. Final review and acceptance of the modification
digital components.  During interviews with station personnel, the inspectors also
    will be performed by the Office of Nuclear Reactor Regulation at a later date.
determined that station engineers received specific training on EMI related to digital
4OA6 Meetings, Including Exit
components.Analysis.  The inspectors determined that the failure of the licensee to adequatelyevaluate the new air conditioning unit with respect to design differences and possibleEMI interactions was a performance deficiency.  The finding was determined to be more
    On October 6, 2006, the inspectors presented the access controls inspection results to
than minor because it affected the design control attribute of the initiating events
    Mr. T. Mitchell, General Manager and other members of his staff who acknowledged the
cornerstone objective to limit the likelihood of those events that upset plant stability and
    findings. The inspectors confirmed that proprietary information was not provided or
challenge critical safety functions during shutdown as well as power operations.  Using theMC 0609, "Significance Determination Process," Phase 1 Worksheet, the finding is
    examined during the inspection.
determined to have very low safety significance because the condition only affected the
    The engineering inspectors presented the results of the inservice inspection review to
initiating events cornerstone and did not contribute to both the likelihood of a reactor trip
    Mr. J. Kowalewski, Director, Engineering, on October 10, 2006. Mr. Kowalewski
and the likelihood that mitigation equipment or functions will not be available.  The cause
    acknowledged the inspection findings. The engineering inspector conducted a followup
of the finding is related to the crosscutting element of problem identification and resolutionassociated with operating experience because the licensee's failure to implement and
    exit with Mr. T. Mitchell, General Manager, Plant Operations, on December 4, 2006, to
institutionalize OE through changes to station processes and procedures.Enforcement.  While a performance deficiency was identified with regard to the trip of theMFP A, there were no violations identified during the review of this issue.  The licensee
    provide updated information on the documentation associated with the review of the
has entered this issue into the CAP as CR ANO-1-2006-1399:  FIN 05000313/2006005-5,
    containment sump modification. The inspectors identified that they had not reviewed
"Trip of a MFP Due to Inadequate Design Control."4OA5Other Activities.1(Closed) Temporary Instruction (TI) 2515/169, Mitigating Systems PerformanceIndex (MSPI) Verification    a.Inspection ScopeDuring this inspection period, the inspectors completed a review of the licensee'simplementation of the MSPI in accordance with the guidance provided in TI 2515/169.
    proprietary information.
The review examined the licensee's MSPI Basis Documents (ANO1-A-6-0001, Revision 1,
    On November 1, 2006, the inspector presented the results of the emergency plan change
and ANO2-SA-06-00001, Revision 0) and verified the established system boundaries and
    inspection to Mr. R. Holeyfield, Supervisor, Emergency Preparedness. The inspector
monitored components were consistent with guidance provided in NEI 99-02, "Reactor
    confirmed that proprietary information was not provided or examined during the
Oversight Process Performance Indicators," Revision 4.  The inspectors verified that the
    inspection.
licensee did not include credit for unavailability hours for "short term unavailability" or
    The resident inspectors presented the inspection results of the resident inspections to
"operator recovery actions to restore the risk-significant function" as is allowed by
    Mr. J. Forbes, Vice President, Operations, and other members of the licensee's
NEI 99-02.
    management staff on January 17, 2007. The resident inspectors conducted a followup
-30-EnclosureAdditionally, the inspectors reviewed the baseline MSPI unavailability time using plantspecific values for the period of 2002 through 2004.  The verification included all planned
    exit with Mr. J. Forbes, Vice President, Operations, on February 8, 2007. The licensee
and unplanned unavailability.  For Unit 1, the inspectors reviewed the baseline MSPI
    acknowledged the findings presented. The inspectors noted that while proprietary
unreliability data using plant specific values for the period of 2002 through 2004.  Unit 2
    information was reviewed, none would be included in this report.
derived its baseline unreliability on industry standard values, as is permitted by NEI 99-02.
ATTACHMENT: SUPPLEMENTAL INFORMATION
The plant specific data for 2005 through 2006 were also reviewed to ensure the licensee
                                              -31-                                   Enclosure
properly accounted for the actual unavailability hours of MSPI systems.  For the same
 
period, the MSPI component unreliability data was examined to ensure the licensee
                                SUPPLEMENTAL INFORMATION
identified all failures of monitored components.  The accuracy and completeness of the
                                  KEY POINTS OF CONTACT
reported unavailability and unreliability data was verified by reviewing operating logs, CRs,
Licensee Personnel
and work order documents.  The unavailability and unreliability data was compared with PI
R. Barnes, Manager, Planning, Scheduling, and Outages
data submitted to the NRC to ensure that any discrepancies would not result in a change
S. Bennett, Project Manager, Licensing
to the index color.    b.FindingsNo findings of significance were identified.  This completes the inspection requirementsfor this TI..2Institute of Nuclear Power Operations Plant Assessment Report Review      a.Inspection ScopeThe inspectors reviewed the final report for the Institute of Nuclear Power Operationsplant assessment of Arkansas Nuclear One, Units 1 and 2, conducted in July and
August 2006. The inspectors reviewed the report to ensure that issues identified were
consistent with the NRC perspectives of licensee performance and to verify if any
significant safety issues were identified that required further NRC followup.      b.FindingsNo findings of significance were identified..3(Closed) Unresolved Item (URI) 05000313/2006003-01, Failure to Retrieve RequiredRecords of Activities Affecting QualityIn response to inspectors questioning the seismic capability of the Tendon SurveillanceCranes L-28 on Unit 1, the licensee could not locate the appropriate documentation.  The
licensee evaluated the as found conditions of the cranes against the uniformed building
code.  The licensee concluded that the cranes would be able to withstand the design
basis earthquake without affecting mitigating equipment.  These evaluations were
reviewed by the inspectors.  No findings of significance were identified, and no violations
of NRC requirements were identified. The licensee documented the evaluations
demonstrating the seismic qualification in CR ANO-1-2005-3109.  This unresolved
item (URI) is closed.
-31-Enclosure.4NRC TI 2515/166, PWR Containment Sump BlockageThe inspectors reviewed ANO's Unit 2 implementation of plant modifications andprocedure changes committed to in their response to Generic Letter 2004-02, "Potential
Impact of Debris on Emergency Recirculation During Design Basis Accidents atPressurized Water Reactors."The inspectors observed installation of the containment recirculation sump strainers,debris barriers, and interceptors.  In addition, the inspectors verified that ANO Unit 2 has
implemented specific procedure changes to control tags, labels, tape, and other objects
inside the containment building.At the time of the inspection, industry testing for chemical effects on containmentrecirculation sumps was not complete.  Since the testing was not complete, ANO Unit 2
evaluated the new recirculation sump modifications to the original design basis,
Regulatory Guide 1.82, "Water Sources for Long-Term Recirculation Cooling Following a
Loss-of-Coolant Accident," Revision 0.  Final review and acceptance of the modification
will be performed by the Office of Nuclear Reactor Regulation at a later date.4OA6Meetings, Including ExitOn October 6, 2006, the inspectors presented the access controls inspection results toMr. T. Mitchell, General Manager and other members of his staff who acknowledged the
findings.  The inspectors confirmed that proprietary information was not provided or
examined during the inspection.The engineering inspectors presented the results of the inservice inspection review toMr. J. Kowalewski, Director, Engineering, on October 10, 2006.  Mr. Kowalewski
acknowledged the inspection findings.  The engineering inspector conducted a followup
exit with Mr. T. Mitchell, General Manager, Plant Operations, on December 4, 2006, to
provide updated information on the documentation associated with the review of the
containment sump modification.  The inspectors identified that they had not reviewed
proprietary information.On November 1, 2006, the inspector presented the results of the emergency plan changeinspection to Mr. R. Holeyfield, Supervisor, Emergency Preparedness.  The inspector
confirmed that proprietary information was not provided or examined during the
inspection.The resident inspectors presented the inspection results of the resident inspections toMr. J. Forbes, Vice President, Operations, and other members of the licensee's
management staff on January 17, 2007.  The resident inspectors conducted a followup
exit with Mr. J. Forbes, Vice President, Operations, on February 8, 2007.  The licensee
acknowledged the findings presented.  The inspectors noted that while proprietary
information was reviewed, none would be included in this report.ATTACHMENT:  SUPPLEMENTAL INFORMATION  
A-1AttachmentSUPPLEMENTAL INFORMATIONKEY POINTS OF CONTACTLicensee PersonnelR. Barnes, Manager, Planning, Scheduling, and OutagesS. Bennett, Project Manager, Licensing
B. Berryman, Manager, Operations Unit 1
B. Berryman, Manager, Operations Unit 1
J. Browning, Manager, Operations Unit 2  
J. Browning, Manager, Operations Unit 2
S. Cotton, Manager, Training
S. Cotton, Manager, Training
B. Daiber, Supervisor, Systems Engineering
B. Daiber, Supervisor, Systems Engineering
J. Eichenberger, Manager, Corrective Actions and Assessments
J. Eichenberger, Manager, Corrective Actions and Assessments
J. Forbes, Vice President, Operations  
J. Forbes, Vice President, Operations
R. Fowler, Emergency Planner
R. Fowler, Emergency Planner
R. Freeman, Emergency Planner
R. Freeman, Emergency Planner
Line 782: Line 1,396:
D. White, Emergency Planner
D. White, Emergency Planner
P. Williams, Supervisor, Systems Engineering
P. Williams, Supervisor, Systems Engineering
M. Woodby, Manager, Design EngineeringLIST OF ITEMS OPENED, CLOSED, AND DISCUSSEDOpened and Closed05000368/2006005-01NCVFire During Hot Work Activities on the Containment SumpStrainer (Section 1R05)05000368/2006005-02NCVFailure to Perform Modification Resulted in an InoperableRCP Oil Collection System (Section 1R15)  
M. Woodby, Manager, Design Engineering
A-2Attachment05000368/2006005-03NCVInadvertent RCS Draining While in Mode 5 (Section 1R20)05000368/2006005-04FINUnplanned Increase in Time with Reactor Vessel Water Levelat Flange Level (Section 1R20)05000313/2006005-05FINTrip of a MFP Due to Inadequate Design Control(Section 4OA3)
                      LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Closed05000313/2006003-01URIFailure to Retrieve Required Records of Activities AffectingQuality (Section 4OA5)
Opened and Closed
Discussed NoneLIST OF DOCUMENTS REVIEWEDIn addition to the documents referred to in the inspection report, the following documents wereselected and reviewed by the inspectors to accomplish the objectives and scope of the inspection
05000368/2006005-01        NCV  Fire During Hot Work Activities on the Containment Sump
and to support any findings:Section 1R01: Adverse Weather ProtectionNUMBERTITLEREVISIONOP-2203.008Natural Emergencies9
                                  Strainer (Section 1R05)
OP-1203.025Natural Emergencies20Section 1R02: Evaluation of Changes, Tests, or ExperimentsEngineering RequestsNUMBERTITLEREVISIONER-ANO-2002-0836-003Pressurizer Replacement 1
05000368/2006005-02        NCV  Failure to Perform Modification Resulted in an Inoperable
ER-ANO-2002-0836-004Original Pressurizer Removal / ReplacementPressurizer Installation
                                  RCP Oil Collection System (Section 1R15)
1ER-ANO-2002-0836-020Replacement Pressurizer Heater Electrical DesignInput 0  
                                                A-1                                  Attachment
A-3AttachmentSection 1R04:  Equipment AlignmentProceduresNUMBERTITLEREVISIONOP-1104.036Emergency Diesel Generator Operations45
 
Op-1107.002ES Electrical System Operations23
05000368/2006005-03      NCV    Inadvertent RCS Draining While in Mode 5 (Section 1R20)
OP-1104.005Reactor Building Spray System Operation46Section 1R05:  Fire ProtectionPlant DrawingsFZ-1038, Sheet 1, Revision 2FZ-2018, Sheet 1, Revision 2ProceduresNUMBERTITLEREVISIONArkansas Nuclear One Fire Hazards Analysis11PFP-U1ANO Prefire Plan (Unit 1) - Section 1B-357-67-U.doc, Section 1B-354-79-U.doc
05000368/2006005-04      FIN    Unplanned Increase in Time with Reactor Vessel Water Level
2PFP-U2ANO Prefire Plan (Unit 2) - Section 2B-335-2040-
                                  at Flange Level (Section 1R20)
JJ.doc 2EN-DC-127Control of Hot Work and Ignition Sources2
05000313/2006005-05      FIN    Trip of a MFP Due to Inadequate Design Control
CRsANO-1-2005-0950ANO-1-2005-1397ANO-2-2005-1724ANO-2-2006-1565ANO-2-2006-1701Section 1R07: Heat Sink PerformanceNUMBERTITLEREVISIONULD-1-SYS-01ANO-1 Emergency Diesel Generator (EDG) System4
                                  (Section 4OA3)
ULD-1-SYS-10ANO-1 Service Water Systems13
Closed
SPEC-6600-M-012Emergency Diesel Generators for ANO Unit 11
05000313/2006003-01      URI    Failure to Retrieve Required Records of Activities Affecting
ER-ANO-2004-0663-000 2004 Unit 1 EDG Thermal Test Results0
                                  Quality (Section 4OA5)
ER-980310 EDG Coolers, E-20A/B, Service Water FlowRequirementsCALC-91-R-2013-01 Service Water Performance Testing Methodology14
Discussed
A-4AttachmentOP-1309.018 EDG Cooler Thermal TestChange 004-02-0Section 1R08: Inservice Inspection (71111.08P)
None
CRs:ANO-2-2005-0916ANO-2-2006-1208ANO-C-2006-1733
                              LIST OF DOCUMENTS REVIEWED
NDEsREPORTCOMPONENT/LOCATIONMETHODBOP-RT-06-055FW-50 (WDR-40631) Drawing No. 2CCA-15-1, Sheet 1Radiographic
In addition to the documents referred to in the inspection report, the following documents were
BOP-RT-06-056FW-51 (WDR-40632) Drawing No. 2CCA-15-1, Sheet 1Radiographic
selected and reviewed by the inspectors to accomplish the objectives and scope of the inspection
ISI-UT-06-0332-73-SWS-R-12B-30R, 2HBC-60-1 between FW-52C &FW-6C1AutomaticUltrasonicISI-UT-06-040FW-50 (WDR-40631) Drawing No. 2CCA-15-1, Sheet 1Ultrasonic
and to support any findings:
ISI-UT-06-042FW-51 (WDR-40632) Drawing No. 2CCA-15-1, Sheet 1UltrasonicProceduresPROCEDURETITLEREVISIONCEP-NDE-0110Program Section for Certification of NDE Personnel2
Section 1R01: Adverse Weather Protection
CEP-NDE-0111Certification of Ultrasonic Personnel in Accordancewith ASME Section XI, Appendix VII
          NUMBER                                      TITLE                            REVISION
1CEP-NDE-0400Ultrasonic Examination0CEP-NDE-0404Manual Ultrasonic Examination of Ferritic PipingWelds (ASME XI)
OP-2203.008                Natural Emergencies                                            9
1CEP-NDE-0423Manual Ultrasonic Examination of Austenitic PipingWelds (ASME XI)
OP-1203.025                Natural Emergencies                                          20
1CEP-NDE-0505Ultrasonic Thickness Examination3
Section 1R02: Evaluation of Changes, Tests, or Experiments
A-5AttachmentWelding Procedures/Qualification RecordsNUMBERTITLEREVISION/DATEPQR 107Manual Gas Tungsten & Shielded Metal ArcWelding (GTAW & SMAW), P-No. 8, SA-312 Type
Engineering Requests
          NUMBER                                      TITLE                          REVISION
ER-ANO-2002-0836-003          Pressurizer Replacement                                     1
ER-ANO-2002-0836-004          Original Pressurizer Removal / Replacement                  1
                              Pressurizer Installation
ER-ANO-2002-0836-020          Replacement Pressurizer Heater Electrical Design            0
                              Input
                                                A-2                                  Attachment
 
Section 1R04: Equipment Alignment
Procedures
        NUMBER                                    TITLE                          REVISION
  OP-1104.036              Emergency Diesel Generator Operations                    45
Op-1107.002              ES Electrical System Operations                          23
OP-1104.005              Reactor Building Spray System Operation                  46
Section 1R05: Fire Protection
Plant Drawings
  FZ-1038, Sheet 1, Revision 2
FZ-2018, Sheet 1, Revision 2
Procedures
        NUMBER                                    TITLE                          REVISION
                          Arkansas Nuclear One Fire Hazards Analysis                11
PFP-U1                    ANO Prefire Plan (Unit 1) - Section 1B-357-67-U.doc,       2
                          Section 1B-354-79-U.doc
PFP-U2                    ANO Prefire Plan (Unit 2) - Section 2B-335-2040-           2
                          JJ.doc
EN-DC-127                Control of Hot Work and Ignition Sources                  2
CRs
ANO-1-2005-0950          ANO-2-2005-1724          ANO-2-2006-1565          ANO-2-2006-1701
ANO-1-2005-1397
Section 1R07: Heat Sink Performance
        NUMBER                                    TITLE                            REVISION
ULD-1-SYS-01              ANO-1 Emergency Diesel Generator (EDG) System                4
ULD-1-SYS-10              ANO-1 Service Water Systems                                13
SPEC-6600-M-012            Emergency Diesel Generators for ANO Unit 1                  1
ER-ANO-2004-0663-000       2004 Unit 1 EDG Thermal Test Results                        0
ER-980310                 EDG Coolers, E-20A/B, Service Water Flow
                            Requirements
CALC-91-R-2013-01         Service Water Performance Testing Methodology              14
                                              A-3                              Attachment
 
OP-1309.018               EDG Cooler Thermal Test                              Change 004-02-0
Section 1R08: Inservice Inspection (71111.08P)
CRs:
ANO-2-2005-0916          ANO-2-2006-1208              ANO-C-2006-1733
NDEs
    REPORT                          COMPONENT/LOCATION                        METHOD
BOP-RT-06-055      FW-50 (WDR-40631) Drawing No. 2CCA-15-1, Sheet 1          Radiographic
BOP-RT-06-056      FW-51 (WDR-40632) Drawing No. 2CCA-15-1, Sheet 1          Radiographic
ISI-UT-06-033      2-73-SWS-R-12B-30R, 2HBC-60-1 between FW-52C &           Automatic
                    FW-6C1                                                    Ultrasonic
ISI-UT-06-040      FW-50 (WDR-40631) Drawing No. 2CCA-15-1, Sheet 1          Ultrasonic
ISI-UT-06-042      FW-51 (WDR-40632) Drawing No. 2CCA-15-1, Sheet 1          Ultrasonic
Procedures
      PROCEDURE                                      TITLE                        REVISION
CEP-NDE-0110              Program Section for Certification of NDE Personnel          2
CEP-NDE-0111              Certification of Ultrasonic Personnel in Accordance        1
                          with ASME Section XI, Appendix VII
CEP-NDE-0400              Ultrasonic Examination                                      0
CEP-NDE-0404              Manual Ultrasonic Examination of Ferritic Piping            1
                          Welds (ASME XI)
CEP-NDE-0423              Manual Ultrasonic Examination of Austenitic Piping          1
                          Welds (ASME XI)
CEP-NDE-0505              Ultrasonic Thickness Examination                            3
                                                A-4                            Attachment
 
Welding Procedures/Qualification Records
        NUMBER                                    TITLE                      REVISION/
                                                                                DATE
PQR 107                  Manual Gas Tungsten & Shielded Metal Arc                1
                          Welding (GTAW & SMAW), P-No. 8, SA-312 Type
                          304
PQR 170                  Manual Gas Tungsten & Shielded Metal Arc                1
                          Welding (GTAW & SMAW), P-No. 8, SA-240 Type
                          304
WPS E-P8-T-A8,Ar          Manual Gas Tungsten Arc Welding (GTAW) of              0
                          P-No. 8 Stainless Steels
WPS E-P8-T(M)-A8,Ar      Machine Gas Tungsten Arc Welding (GTAW) of              0
                          P-No. 8 Stainless Steels
WP 06-121                2T-1 Surge Line                                    October 3,
                                                                                2006
Section 1R13: Maintenance Risk Assessments and Emergent Work Control
COPD-024, Risk Assessment Guidelines, Revision 18
Section 1R15: Operability Evaluations
CRs
ANO-2-1995-0555          ANO-2-2006-1459            ANO-2-2006-1522    ANO-2-2006-1796
ANO-2-2006-1407          ANO-2-2006-1478            ANO-2-2006-1539    ANO-2-2006-1853
ANO-2-2006-1433          ANO-2-2006-1521            ANO-2-2006-1757    ANO-2-2006-1879
Procedure
OP-2305.002, Reactor Coolant System Leak Detection, Revision 14
Engineering Requests
ER-ANO-2000-2528-003, ANO Sump Operability when the RCS Temperature is Above 200 F
ER-ANO-2004-0060-000, ANO-2 Sump Operability for the RCS Temperature above 200 F
Miscellaneous Documents
2CNA108802, Safety Evaluation Report, dated October 26, 1988
0CAN088404, Station Letter to USNRC Requesting Exemption, dated August 15, 1984
                                              A-5                            Attachment
 
Section 1R17: Permanent Plant Modifications
Engineering Requests
        NUMBER                                    TITLE
ER-ANO-2002-0836-003      Pressurizer Replacement
ER-ANO-2002-0836-004      Original Pressurizer Removal / Replacement
                          Pressurizer Installation
ER-ANO-2002-0836-005      Interference Removal / Reinstallation Inside the
                          Pressurizer Cubicle
ER-ANO-2002-0836-006      Interference Removal / Reinstallation Outside the
                          Pressurizer Cubicle
ER-ANO-2002-0836-007      ANO-2 Pressurizer Replacement Rigging and
                          Handling
ER-ANO-2002-0836-020      Replacement Pressurizer Heater Electrical Design
                          Input
Section 1R20: Refueling and Outage Activities
Procedures
        NUMBER                                      TITLE                        REVISION
OP-2104.004              Shutdown Cooling System                                  031-00-0
OP-2104.019              Clean Resin Transfer                                    009-01-0
OP-2504.005              Reactor Vessel Closure Head Removal                      012-01-0
Miscellaneous Document
Shutdown Operations Protection Plan, dated August 4, 2005
CRs
ANO-2-2006-1464        ANO-2-2006-1573            ANO-2-2006-2032          ANO-C-2006-1678
ANO-2-2006-1553        ANO-2-2006-1734            ANO-C-2006-1473
Section 2OS1: Access Controls to Radiologically Significant Areas
CRs
ANO-1-2006-0479        ANO-2-2006-1434            ANO-2-2006-1497        ANO-2-2006-1568
ANO-1-2006-0700        ANO-2-2006-1446            ANO-2-2006-1501        ANO-2-2006-1568
ANO-1-2006-1113        ANO-2-2006-1471            ANO-2-2006-1511        ANO-2-2006-1575
ANO-2-2005-1429        ANO-2-2006-1495            ANO-2-2006-1523        ANO-2-2006-1598
                                              A-6                                Attachment


304 1PQR 170Manual Gas Tungsten & Shielded Metal ArcWelding (GTAW & SMAW), P-No. 8, SA-240 Type
ANO-2-2006-1606          ANO-2-2006-1674            ANO-2-2006-1716        ANO-2-2006-1774
ANO-2-2006-1636          ANO-2-2006-1675            ANO-2-2006-1717        ANO-2-2006-1790
ANO-2-2006-1638          ANO-2-2006-1695            ANO-2-2006-1748        ANO-C-2006-1698
ANO-2-2006-1671          ANO-2-2006-1696            ANO-2-2006-1765
Audits and Self-Assessments
Self-Assessment Report, QS-2006-ANO-007, 2R18 Radiation Protection Outage Planning
Review
Radiation Work Permits
        NUMBER                                      TITLE
RWP 2006-2420            Scaffold Activities
RWP 2006-2501            Support Activities for Pressurizer Replacement
RWP 2006-2502            Remove and Replace Pressurizer
RWP 2006-2520            Incore Instrument Thimble Tube Replacement
RWP 2005-2530            Sump Screen Modification
RWP 2006-2540            Hot Leg RTD Replacement
Procedures
        NUMBER                                      TITLE                        REVISION
1601.209                  Whole Body Counting/Bioassay                          CHANGE
                                                                                  009-00
EN-RP-104                Personnel Contamination Events                            3
EN-RP-108                Radiation Protection Posting                              3
EN-RP-131                Air Sampling                                              1
EN-RP-203                Dose Assessment                                          0
EN-RP-208                Whole Body Counting and In-Vitro Bioassay                0
PL-182                    Radiation Protection Expectations and Standards          1
Miscellaneous Document
Alpha Monitoring Plan, Revised August 22, 2006
                                              A-7                              Attachment


304 1WPS E-P8-T-A8,ArManual Gas Tungsten Arc Welding (GTAW) ofP-No. 8 Stainless Steels
Section 4OA2: Identification and Resolution of Problems
0WPS E-P8-T(M)-A8,ArMachine Gas Tungsten Arc Welding (GTAW) ofP-No. 8 Stainless Steels
CRs
0WP 06-1212T-1 Surge LineOctober 3, 2006Section 1R13: Maintenance Risk Assessments and Emergent Work ControlCOPD-024, "Risk Assessment Guidelines," Revision 18Section 1R15:  Operability Evaluations
ANO-2-2006-1535          ANO-2-2006-1655          ANO-2-2006-1891
CRsANO-2-1995-0555ANO-2-2006-1407
ANO-2-2006-1625          ANO-2-2006-1693          ANO-2-2006-2174
ANO-2-2006-1433ANO-2-2006-1459ANO-2-2006-1478
Section 4OA3: Event Follow-up
ANO-2-2006-1521ANO-2-2006-1522ANO-2-2006-1539
Procedures
ANO-2-2006-1757ANO-2-2006-1796ANO-2-2006-1853
        NUMBER                                    TITLE                REVISION
ANO-2-2006-1879ProcedureOP-2305.002, "Reactor Coolant System Leak Detection," Revision 14
  EN-DC-141                  Design Inputs                                    2
Engineering RequestsER-ANO-2000-2528-003, "ANO Sump Operability when the RCS Temperature is Above 200 F"ER-ANO-2004-0060-000, "ANO-2 Sump Operability for the RCS Temperature above 200 F"Miscellaneous Documents2CNA108802, "Safety Evaluation Report," dated October 26, 19880CAN088404, "Station Letter to USNRC Requesting Exemption," dated August 15, 1984
  EN-DC-313                  Procurement Engineering Process                  0
A-6AttachmentSection 1R17: Permanent Plant ModificationsEngineering RequestsNUMBERTITLEER-ANO-2002-0836-003Pressurizer Replacement
CRs
ER-ANO-2002-0836-004Original Pressurizer Removal / ReplacementPressurizer InstallationER-ANO-2002-0836-005Interference Removal / Reinstallation Inside thePressurizer CubicleER-ANO-2002-0836-006Interference Removal / Reinstallation Outside thePressurizer CubicleER-ANO-2002-0836-007ANO-2 Pressurizer Replacement Rigging and
ANO-1-2006-1399          ANO-2-2006-1464          ANO-2-2006-2444 ANO-2-2006-2449
HandlingER-ANO-2002-0836-020Replacement Pressurizer Heater Electrical DesignInputSection 1R20: Refueling and Outage ActivitiesProceduresNUMBERTITLEREVISIONOP-2104.004Shutdown Cooling System031-00-0
Section 4OA5: Other Activities (TI 2515/0166)
OP-2104.019Clean Resin Transfer009-01-0
Safety Evaluation
OP-2504.005Reactor Vessel Closure Head Removal012-01-0Miscellaneous DocumentShutdown Operations Protection Plan, dated August 4, 2005
FFN-06-008, Unit 2 RBS/ECCS Sump Strainer Replacement
CRsANO-2-2006-1464ANO-2-2006-1553ANO-2-2006-1573ANO-2-2006-1734ANO-2-2006-2032ANO-C-2006-1473ANO-C-2006-1678Section 2OS1:  Access Controls to Radiologically Significant Areas
                                              A-8                      Attachment
CRsANO-1-2006-0479ANO-1-2006-0700
ANO-1-2006-1113
ANO-2-2005-1429ANO-2-2006-1434ANO-2-2006-1446
ANO-2-2006-1471
ANO-2-2006-1495ANO-2-2006-1497ANO-2-2006-1501
ANO-2-2006-1511
ANO-2-2006-1523ANO-2-2006-1568ANO-2-2006-1568
ANO-2-2006-1575
ANO-2-2006-1598
A-7AttachmentANO-2-2006-1606ANO-2-2006-1636
ANO-2-2006-1638
ANO-2-2006-1671ANO-2-2006-1674ANO-2-2006-1675
ANO-2-2006-1695
ANO-2-2006-1696ANO-2-2006-1716ANO-2-2006-1717
ANO-2-2006-1748
ANO-2-2006-1765ANO-2-2006-1774ANO-2-2006-1790
ANO-C-2006-1698Audits and Self-AssessmentsSelf-Assessment Report, "QS-2006-ANO-007, 2R18 Radiation Protection Outage PlanningReview"Radiation Work PermitsNUMBERTITLERWP 2006-2420Scaffold Activities
RWP 2006-2501Support Activities for Pressurizer Replacement
RWP 2006-2502Remove and Replace Pressurizer
RWP 2006-2520Incore Instrument Thimble Tube Replacement
RWP 2005-2530Sump Screen Modification
RWP 2006-2540Hot Leg RTD Replacement ProceduresNUMBERTITLEREVISION1601.209Whole Body Counting/BioassayCHANGE009-00EN-RP-104Personnel Contamination Events3
EN-RP-108Radiation Protection Posting3
EN-RP-131Air Sampling1
EN-RP-203Dose Assessment0
EN-RP-208Whole Body Counting and In-Vitro Bioassay0
PL-182Radiation Protection Expectations and Standards1Miscellaneous DocumentAlpha Monitoring Plan, Revised August 22, 2006
A-8AttachmentSection 4OA2:  Identification and Resolution of Problems
CRsANO-2-2006-1535ANO-2-2006-1625ANO-2-2006-1655ANO-2-2006-1693ANO-2-2006-1891ANO-2-2006-2174Section 4OA3:  Event Follow-upProceduresNUMBERTITLEREVISIONEN-DC-141Design Inputs2
EN-DC-313Procurement Engineering Process0
CRsANO-1-2006-1399ANO-2-2006-1464ANO-2-2006-2444ANO-2-2006-2449Section 4OA5: Other Activities (TI 2515/0166)Safety EvaluationFFN-06-008, "Unit 2 RBS/ECCS Sump Strainer Replacement"
A-9AttachmentLIST OF ACRONYMSANOArkansas Nuclear OneASMEAmerican Society of Mechanical Engineers Boiler and Pressure Vessel Code
CAPcorrective action program
CCWcomponent cooling water


CFRCode of Federal RegulationsCRcondition report
                            LIST OF ACRONYMS
DSMdigital speed monitor
ANO  Arkansas Nuclear One
EDGemergency diesel generator
ASME  American Society of Mechanical Engineers Boiler and Pressure Vessel Code
EMIelectromagnetic interference
CAP  corrective action program
FINfinding
CCW  component cooling water
MCmanual chapter
CFR  Code of Federal Regulations
MFPmain feedwater pump
CR    condition report
MSPImitigating systems performance index
DSM  digital speed monitor
NCVnoncited violation
EDG  emergency diesel generator
NDEnondestructive examination
EMI  electromagnetic interference
PIperformance indicator
FIN  finding
PWRpressurized water reactor
MC    manual chapter
RCPreactor coolant pump
MFP  main feedwater pump
RCSreactor coolant system
MSPI  mitigating systems performance index
RTPrated thermal power
NCV  noncited violation
SSCssystem, structure, and components
NDE  nondestructive examination
TItemporary instruction
PI    performance indicator
TSTechnical Specification
PWR  pressurized water reactor
UFSARUpdated Final Safety Analysis
RCP  reactor coolant pump
URIunresolved item
RCS  reactor coolant system
RTP  rated thermal power
SSCs  system, structure, and components
TI    temporary instruction
TS    Technical Specification
UFSAR Updated Final Safety Analysis
URI  unresolved item
                                    A-9                                Attachment
}}
}}

Revision as of 09:24, 23 November 2019

IR 05000313-06-005 and 05000368-06-005 for Arkansas Nuclear One
ML070450249
Person / Time
Site: Arkansas Nuclear  Entergy icon.png
Issue date: 02/14/2007
From: Clark J
NRC/RGN-IV/DRP/RPB-E
To: Forbes J
Entergy Operations
References
IR-06-005
Download: ML070450249 (44)


See also: IR 05000313/2006005

Text

February 14, 2007

Jeffrey S. Forbes, Vice President,

Operations

Arkansas Nuclear One

Entergy Operations, Inc.

1448 S.R. 333

Russellville, Arkansas 72801-0967

SUBJECT: ARKANSAS NUCLEAR ONE - NRC INTEGRATED INSPECTION REPORT

05000313/2006005 AND 05000368/2006005

Dear Mr. Forbes:

On December 31, 2006, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at your Arkansas Nuclear One, Units 1 and 2, facility. The enclosed integrated

report documents the inspection findings, which were discussed on January 17, 2007, and

again on February 8, 2007, with you and other members of your staff.

The inspection examined activities conducted under your licenses as they relate to safety and

compliance with the Commission's rules and regulations and with the conditions of your

licenses. The inspectors reviewed selected procedures and records, observed activities, and

interviewed personnel.

The report documents five self-revealing findings of very low safety significance (Green). Three

of these findings were determined to involve violations of NRC requirements. However,

because of the very low safety significance and because they are entered into your corrective

action program, the NRC is treating these findings as noncited violations consistent with

Section VI.A.1 of the NRC Enforcement Policy. If you contest these noncited violations, you

should provide a response within 30 days of the date of this inspection report, with the basis for

your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,

Washington DC 20555-0001; with copies to the Regional Administrator, U.S. Nuclear

Regulatory Commission Region IV, 611 Ryan Plaza Drive, Suite 400, Arlington, Texas

76011-4005; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission,

Washington DC 20555-0001; and the NRC Resident Inspector at Arkansas Nuclear One,

Units 1 and 2, facility.

In accordance with 10 CFR 2.390 of the NRC's Rules of Practice, a copy of this letter, its

enclosure, and your response (if any) will be made available electronically for public inspection

Entergy Operations, Inc. -2-

in the NRC Public Document Room or from the Publicly Available Records (PARS) component

of NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Jeffrey A. Clark, Chief

Project Branch E

Division of Reactor Projects

Dockets: 50-313

50-368

Licenses: DPR-51

NPF-6

Enclosure:

NRC Inspection Report 05000313/2006005 and 05000368/2006005

w/Attachment: Supplemental Information

cc w/Enclosure:

Senior Vice President

& Chief Operating Officer

Entergy Operations, Inc.

P.O. Box 31995

Jackson, MS 39286-1995

Vice President

Operations Support

Entergy Operations, Inc.

P.O. Box 31995

Jackson, MS 39286-1995

General Manager Plant Operations

Entergy Operations, Inc.

Arkansas Nuclear One

1448 S. R. 333

Russellville, AR 72802

Director, Nuclear Safety Assurance

Entergy Operations, Inc.

Arkansas Nuclear One

1448 S. R. 333

Russellville, AR 72802

Entergy Operations, Inc. -3-

Manager, Licensing

Entergy Operations, Inc.

Arkansas Nuclear One

1448 S. R. 333

Russellville, AR 72802

Director, Nuclear Safety & Licensing

Entergy Operations, Inc.

1340 Echelon Parkway

Jackson, MS 39213-8298

Section Chief, Division of Health

Radiation Control Section

Arkansas Department of Health and

Human Services

4815 West Markham Street, Slot 30

Little Rock, AR 72205-3867

Section Chief, Division of Health

Emergency Management Section

Arkansas Department of Health and

Human Services

4815 West Markham Street, Slot 30

Little Rock, AR 72205-3867

Manager, Washington Nuclear Operations

ABB Combustion Engineering Nuclear

Power

12300 Twinbrook Parkway, Suite 330

Rockville, MD 20852

County Judge of Pope County

Pope County Courthouse

100 West Main Street

Russellville, AR 72801

James Mallay

Director, Regulatory Affairs

Framatome ANP

3815 Old Forest Road

Lynchburg, VA 24501

Entergy Operations, Inc. -4-

Electronic distribution by RIV:

Regional Administrator (BSM1)

DRP Director (ATH)

DRS Director (DDC)

DRS Deputy Director (RJC1)

Senior Resident Inspector (RWD)

Branch Chief, DRP/E (ZKD)

Senior Project Engineer, DRP/E (VGG)

Team Leader, DRP/TSS (RLN1)

RITS Coordinator (MSH3)

DRS STA (DAP)

D. Cullison, OEDO RIV Coordinator (DGC)

ROPreports

ANO Site Secretary (VLH)

SUNSI Review Completed: _JAC__ ADAMS: / Yes No Initials: __JAC____

/ Publicly Available G Non-Publicly Available G Sensitive / Non-Sensitive

R:\_REACTORS\_ANO\2006\AN2006-05RP-RWD.wpd

RIV:RI:DRP/E RI:DRP/E SRI:DRP/E C:DRS/OB

CHYoung JEJosey RWDeese ATGody

T-JAC T-JAC T-JAC /RA/

2/5/2007 2/5/2007 2/5/2007 2/4/2007

C:DRS/PSB C:DRS/EB1 C:DRS/EB2 C:DRP/E

MPShannon WBJones LJSmith JAClark

/RA/ /RA/ /RA/ /RA/

2/5/2007 2/1/2007 2/1/2007 2/14/2007

OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Dockets: 50-313, 50-368

Licenses: DPR-51, NPF-6

Report: 05000313/2006005 and 05000368/2006005

Licensee: Entergy Operations, Inc.

Facility: Arkansas Nuclear One, Units 1 and 2

Location: Junction of Hwy. 64W and Hwy. 333 South

Russellville, Arkansas

Dates: September 24 through December 31, 2006

Inspectors: L. Carson II, Senior Health Physicist, Plant Support Branch

R. Deese, Senior Resident Inspector

J. Josey, Resident Inspector

J. Kirkland, Project Engineer

R. Lantz, Senior Emergency Preparedness Inspector

D. Livermore, Senior Project Engineer

C. Paulk, Senior Reactor Inspector

C. Young, Resident Inspector

Accompanying

Personnel: S. Makor, Reactor Inspector

Approved By: Jeffrey A. Clark, Chief, Project Branch E

Division of Reactor Projects

-1- Enclosure

TABLE OF CONTENTS

SUMMARY OF FINDINGS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3

1R01 Adverse Weather Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6

1R02 Evaluation of Changes, Tests, or Experiments . . . . . . . . . . . . . . . . . . . . . . . . . 7

1R04 Equipment Alignment . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7

1R05 Fire Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7

1R07 Heat Sink Performance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 10

1R08 Inservice Inspection Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 10

1R11 Licensed Operator Requalification Program . . . . . . . . . . . . . . . . . . . . . . . . . . . 13

1R12 Maintenance Effectiveness . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 13

1R13 Maintenance Risk Assessments and Emergent Work Control . . . . . . . . . . . . . 14

1R15 Operability Evaluations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 15

1R17 Permanent Plant Modifications . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17

1R19 Postmaintenance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17

1R20 Refueling and Outage Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 18

1R22 Surveillance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 21

1EP4 Emergency Action Level and Emergency Plan Changes . . . . . . . . . . . . . . . . . 22

1EP6 Drill Evaluation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 22

RADIATION SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 23

2OS1 Access Control To Radiologically Significant Areas . . . . . . . . . . . . . . . . . . . . . 23

OTHER ACTIVITIES . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 24

4OA1 PI Verification . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 24

4OA2 Identification and Resolution of Problems . . . . . . . . . . . . . . . . . . . . . . . . . . . . 25

4OA3 Followup of Events and Notices of Enforcement Discretion . . . . . . . . . . . . . . 28

4OA5 Other Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 29

4OA6 Meetings, Including Exit . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 31

SUPPLEMENTAL INFORMATION . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

KEY POINTS OF CONTACT . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

LIST OF DOCUMENTS REVIEWED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-2

LIST OF ACRONYMS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-9

-2- Enclosure

SUMMARY OF FINDINGS

IR 05000313/2006005, 05000368/2006005; 09/24/2006 - 12/31/2006; Arkansas Nuclear One,

Units 1 and 2; Fire Protection, Operability Evaluations, Refueling and Outage Activities, Follow-

up of Events and Notices of Enforcement Discretion.

This report covered a 3-month period of inspection by resident and regional specialist

inspectors. Five Green findings, three of which were noncited violations were identified. The

significance of most findings is indicated by their color (Green, White, Yellow, or Red) using

Inspection Manual Chapter 0609, Significance Determination Process. Findings for which the

significance determination process does not apply may be Green or be assigned a severity

level after NRC management's review. The NRCs program for overseeing the safe operation

of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight

Process, Revision 3, dated July 2000.

A. NRC-Identified and Self-Revealing Findings

Cornerstone: Initiating Events

  • Green. A self-revealing noncited violation of Unit 2 Technical

Specification 6.4.1.c, Fire Protection Program Implementation, was identified for

the failure of maintenance personnel to follow Procedure EN-DC-127, Control of

Hot Work and Ignition Sources, while performing hot work. Specifically, the

licensee failed to ensure that combustible material within 35 feet of the work area

was removed or protected. Consequently, torch cutting activities near the Unit 2

containment sump strainer caused a nearby plastic bag containing used

protective clothing to ignite. This issue was entered into the licensee's

corrective action program as Condition Reports ANO-2-2006-1565 and Condition

Report ANO-2-2006-1701. A number of additional examples of hot work

activities that involved inadequate implementation of applicable hot work control

procedures were also identified.

The finding is greater than minor because it is associated with the protection

against external factors attribute of the initiating events cornerstone, and it

directly affects the cornerstone objective to limit the likelihood of those events

that upset plant stability and challenge critical safety functions during shutdown

as well as power operations. Additionally, if left uncorrected, the practice of

conducting hot work in a manner that results in unintended combustion of nearby

materials would become a more significant safety concern in that it could result

in a fire in or near other risk important equipment. The finding is not suitable for

evaluation with the significance determination process neither the fire protection

significance determination process nor the shutdown operations significance

determination process address shutdown fire protection findings. However, the

finding is determined to be of very low safety significance by NRC managements

review because the finding occurred while the unit was already in a cold

shutdown condition, and the operability of equipment necessary to maintain safe

-3- Enclosure

shutdown was not challenged. The cause of the finding is related to the

crosscutting element of human performance associated with work practices

because the fire watch failed to use error prevention techniques like self

checking and peer checking which would have prevented the event

(Section 1R05).

  • Green. A self-revealing noncited violation of Unit 2 Technical

Specification 6.4.1.a, Procedures, was identified when an operator failed to

close Valve 2DCH-11, resin sluice header drain valve, when securing from a

resin transfer as required by procedure. One week later, while aligning the plant

for alternate purification with Valve 2DCH-11 being out of position, an

unanticipated loss of approximately 230 gallons of reactor coolant system

inventory occurred. This issue was entered into the licensee's corrective action

program as Condition Report ANO-2-2006-1464.

The finding was determined to be more than minor because it affected the

configuration control attribute of the initiating events cornerstone objective to limit

the likelihood of those events that upset plant stability and challenge critical

safety functions during shutdown as well as power operations. Using the

shutdown operations significance determination process, the finding was

determined to have very low safety significance because the finding did not

result in a loss of 2 feet or more of reactor coolant system inventory and did not

result in a loss of reactor coolant system inventory while in reduced inventory.

The cause of the finding is related to the crosscutting element of human

performance associated with work practices because the operator failed to use

error prevention techniques like self checking and peer checking which would

have prevented the event (Section 1R20).

  • Green. A self-revealing finding was identified associated with the licensees

practice of using a hammer to remove the main hook pin on the Unit 2 polar

crane. Specifically, the license failure to provide clear guidance and training

resulted in station personnel cold working by the main hook and load cell pins

and this practice resulted in both pins being deformed and not usable with

reactor vessel level lowered to just below reactor vessel flange level. As a result,

Unit 2 was exposed to an increased period of elevated likelihood of a loss of

decay heat removal while the unit remained in a lowered vessel level condition

for an additional unplanned 27 hours3.125e-4 days <br />0.0075 hours <br />4.464286e-5 weeks <br />1.02735e-5 months <br />. This issue was entered into the licensee's

corrective action program as Condition Report ANO-2-2006-1553.

The finding was determined to be more than minor because it affected the

equipment performance attribute of the initiating events cornerstone objective to

limit the likelihood of those events that upset plant stability and challenge critical

safety functions during shutdown as well as power operations. This finding was

determined to be a finding of very low safety significance using the shutdown

operations significance determination process because the event did not involve

a loss of shutdown control or a reduction in mitigation capability which would

have increased the frequency of occurrence of a loss of decay heat removal.

-4- Enclosure

The cause of this finding is related to the crosscutting element of human

performance associated with resources because the training of personnel and

procedural guidance available was adequate (Section 1R20).

  • Green. A self-revealing finding was identified when the Unit 1 main feedwater

Pump A tripped, resulting in a plant run back to 40 percent reactor power. The

trip occurred due to electromagnetic interference from an air conditioning unit

recently installed on top of the main feedwater pump cabinet. This interference

caused an overspeed trip signal on the digital speed monitor for the main

feedwater pump turbine when no such actual condition occurred. This issue was

entered into the licensee's corrective action program as Condition

Report ANO-1-2006-1399.

The finding was determined to be more than minor because it affected the

design control attribute of the initiating events cornerstone objective to limit the

likelihood of those events that upset plant stability and challenge critical safety

functions during shutdown as well as power operations. Using Manual

Chapter 0609, Significance Determination Process, Phase 1 Worksheet, the

finding is determined to have very low safety significance because the condition

only affected the initiating events cornerstone and did not contribute to both the

likelihood of a reactor trip and the likelihood that mitigation equipment or

functions will not be available. The finding had crosscutting aspects in the area

of problem identification and resolution associated with operating experience

because the licensees failure to implement and institutionalize OE through

changes to station processes and procedures (Section 4OA3).

Cornerstone: Mitigating Systems

  • Green. A self-revealing noncited violation of ANO Unit 2 License

Condition 2.C.(3)(b), Fire Protection, was identified for failure of the licensee to

maintain the lube oil collection system for Reactor Coolant Pumps C and D in an

operable condition. Specifically, the licensee failed to perform a modification on

the motor installed on Reactor Coolant Pump C which resulted in the oil

collection tank and its associated overfill berm being filled with water from the

component cooling water system. This issue was entered into the licensee's

corrective action program as Condition Report ANO-2-2006-1407.

The finding was determined to be more than minor because it affected the

protection against external factors attribute of the mitigating systems cornerstone

objective to ensure the availability, reliability, and capability of systems that

respond to initiating events to prevent undesirable consequences. Using the fire

protection significance determination process, the finding is determined to have

very low safety significance because the condition constituted a low degradation

of a fire prevention and administrative controls feature (Section 1R15).

B. Licensee-Identified Violations

None.

-5- Enclosure

REPORT DETAILS

Summary of Plant Status

Unit 1 began the inspection period at 100 percent rated thermal power (RTP) and remained

there until November 9, 2006, when a trip of the Main Feedwater Pump A occurred due to a

malfunction associated with the electronic overspeed trip device. The trip resulted in an

automatic runback to 40 percent RTP. Unit 1 returned to 100 percent RTP on

November 10 and remained there for the remainder of the inspection period.

Unit 2 began the inspection period with the reactor shut down for Refueling Outage 2R18.

Following the refueling outage, the Unit 2 reactor achieved criticality on October 27 and main

generator output breakers were closed on October 28. Approximately 67 percent RTP was

achieved on October 30 when the unit performed a Technical Specification (TS) required

shutdown to hot standby in response to a fire in 480-volt Motor-Control Center 2B-53. Unit 2

was restarted, and main generator output breakers were closed on November 1. The unit

achieved 100 percent RTP on November 3 and remained there for the remainder of the

inspection period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity

1R01 Adverse Weather Protection (71111.01)

.1 Readiness for Impending Adverse Weather Conditions

On November 30 the inspectors completed a review of the licensee's readiness for

impending adverse weather involving icy weather. The inspectors: (1) reviewed plant

procedures, the Updated Final Safety Analysis Reports (UFSAR), and TSs to ensure

that operator actions defined in adverse weather procedures maintained the readiness

of essential systems; (2) walked down portions of the below listed two systems to

ensure that adverse weather protection features (heat tracing, space heaters,

weatherized enclosures, temporary chillers) were sufficient to support operability,

including the ability to perform safe shutdown functions; (3) reviewed maintenance

records to determine that applicable surveillance requirements were current before the

anticipated ice storm developed; and (4) reviewed plant modifications, procedure

revisions, and operator work arounds to determine if recent facility changes challenged

plant operation.

C November 30, 2006, Units 1 and 2, offsite electrical distribution systems

Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed one sample.

-6- Enclosure

1R02 Evaluation of Changes, Tests, or Experiments (71111.02)

a. Inspection Scope

The inspectors reviewed the effectiveness of the licensees implementation of changes

to the facility structures, systems, and components (SSCs); risk-significant normal and

emergency operating procedures; test programs; and the UFSAR in accordance with

10 CFR 50.59, Changes, Tests, and Experiments. The inspectors reviewed the safety

evaluations performed by the licensee dealing with the Unit 2 pressurizer replacement.

The evaluations were reviewed to verify that licensee personnel had appropriately

considered the conditions under which the licensee may make changes to the facility or

procedures or conduct tests or experiments without prior NRC approval. Procedures,

evaluations, screenings, and applicability determinations reviewed are listed in the

attachment to this report.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment (71111.04)

.1 Partial Walkdown

The inspectors: (1) walked down portions of the two below listed risk important systems

and reviewed plant procedures and documents to verify that critical portions of the

selected systems were correctly aligned, and (2) compared deficiencies identified during

the walkdown to the licensees UFSAR and corrective action program (CAP) to ensure

problems were being identified and corrected.

  • December 13, 2006, Unit 1, reactor building spray system Train A

Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed two samples.

b. Findings

No findings of significance were identified.

1R05 Fire Protection (71111.05)

.1 Quarterly Inspection

The inspectors walked down the six below listed plant areas to assess the material

condition of active and passive fire protection features and their operational lineup and

readiness. The inspectors: (1) verified that transient combustibles and hot work

activities were controlled in accordance with plant procedures; (2) observed the

condition of fire detection devices to verify they remained functional; (3) observed fire

-7- Enclosure

suppression systems to verify they remained functional and that access to manual

actuators was unobstructed; (4) verified that fire extinguishers and hose stations were

provided at their designated locations and that they were in a satisfactory condition;

(5) verified that passive fire protection features (electrical raceway barriers, fire doors,

fire dampers steel fire proofing, penetration seals, and oil collection systems) were in a

satisfactory material condition; (6) verified that adequate compensatory measures were

established for degraded or inoperable fire protection features and that the

compensatory measures were commensurate with the significance of the deficiency;

and (7) reviewed the UFSAR to determine if the licensee identified and corrected fire

protection problems.

  • September 25, 2006, Unit 2, Fire Zone 2032-K, containment building (south side)
  • October 17, 2006, Unit 1, Fire Zone 98-J, EDG access corridor
  • December 13, 2006, Unit 1, Fire Zones 4-EE, 12-EE, and 14-EE, Elevation 317

feet of the auxiliary building, west decay heat removal pump room

  • December 26, 2006, Unit 2, Fire Zone 2040-JJ, access corridor; charging pump;

radwaste and boron management system area

  • December 27, 2006, Unit 1, Fire Zone 67-U, lab and demineralizer access area
  • December 27, 2006, Unit 1, Fire Zone 79-U, upper north piping penetration room

Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed six samples.

b. Findings

Introduction. A self-revealing, Green noncited violation of TS 6.4.1.c was identified for

the licensees failure to adequately implement their procedure for the control of hot work

and ignition sources while performing hot work activities.

Description. On September 25, 2006, hot work activities were being performed on the

Unit 2 containment sump strainer. A plastic bag was being utilized at a nearby step-off

pad at the high contamination area boundary as a receptacle for used protective

clothing. While torch cutting on the west containment sump strainer door was in

progress, sparks from the activity caused the plastic bag to ignite. The inspectors

identified the fire to the firewatch, who was in the vicinity. The bag was extinguished by

smothering soon thereafter by the workers that were involved in the hot work activity.

Procedure EN-DC-127, Control of Hot Work and Ignition Sources, Revision 2, requires

that combustible material within 35 feet of the work area that could become ignited from

the hot work shall be removed or protected. Procedure EN-DC-127, Attachment 9.1,

Hot Work Permit, was issued for this activity and showed that this requirement to be

checked off by the hot work supervisor as being completed. The inspectors noted that

the bag was within 35 feet of the work area and had not been removed.

-8- Enclosure

Corrective actions that were taken by the licensee in response to this event to prevent

recurrence included: moving the step-off pad farther away from the work area, clearing

the area near the door of unnecessary equipment and materials, coaching the firewatch

and his supervisor concerning the responsibility of the firewatch and how to deal with

distractions, discussing alternatives to more effectively contain sparks from the cutting

operation, discussing the event with craft personnel, and conducting more frequent area

inspections.

A number of additional deficiencies were identified through a review of recent licensee

performance in the conduct of related hot work activities. Section 4OA2 of this

enclosure contains some details of other instances that occurred during the Unit 2

Refueling Outage 2R18. Also, three examples involving circumstances similar to the

subject of this finding occurred during the prior refueling outages for each of the two

units. On March 25, 2005, fallen welding slag caused the smoldering of debris below

Containment Cooler D inside the Unit 2 containment building. On September 29 torch

cutting resulted in falling hot metal and slag that caused combustible materials in the

work area to catch on fire. On October 14 three small fires of trash bags containing

combustible materials in the Unit 1 turbine building basement were caused by hot work

activities that were being performed on the levels above. There was no firewatch posted

on the basement level.

Each of these instances was entered into the licensees CAP. These occurrences

represent instances of inadequate implementation of applicable hot work control

procedures. The inspectors concluded that the recent increase in the number of related

findings when compared to past occurrences represented a trend which, if left

uncorrected, could become a more significant safety concern in that it could result in a

fire in or near risk important equipment.

Analysis. The performance deficiency associated with this finding involved the failure of

maintenance personnel to adequately implement the licensees procedure for control of

hot work and ignition sources. The finding is greater than minor because it is

associated with the protection against external factors attribute of the initiating events

cornerstone, and affects the cornerstone objective to limit the likelihood of those events

that upset plant stability and challenge critical safety functions during shutdown as well

as power operations. Additionally, if left uncorrected, the practice of conducting hot

work in a manner that results in unintended combustion of nearby materials would

become a more significant safety concern in that it could result in a fire in or near risk

important equipment. Manual Chapter (MC) 0609, Significance Determination

Process, Appendix F, Fire Protection Significance Determination Process, does not

address the potential risk significance of shutdown fire protection findings. Additionally,

MC 0609, Appendix G, Shutdown Operations Significance Determination Process,

does not address fire protection findings. Thus, the finding is not suitable for

significance determination process evaluation, but has been reviewed by NRC

management and is determined to be of very low safety significance because the finding

occurred while the unit was already in a cold shutdown condition; and the operability of

equipment necessary to maintain safe shutdown was not challenged. The cause of the

finding is related to the crosscutting element of human performance in that maintenance

personnel failed to follow procedures.

-9- Enclosure

Enforcement. Unit 2 TS 6.4, Procedures, requires that written procedures be

established, implemented, and maintained covering fire protection program

implementation. Procedure EN-DC-127, Control of Hot Work and Ignition Sources, is

one of those procedures and requires that combustible material within 35 feet of the

work area that could become ignited from the hot work shall be removed or protected.

Contrary to this, on September 25, 2006, maintenance personnel failed to remove or

protect combustible material within 35 feet of the work area. Because the finding is of

very low safety significance and has been entered into the licensees CAP as Condition

Reports (CRs) ANO-2-2006-1565 and CR ANO-2-2006-1701, this violation is being

treated as an NCV consistent with Section VIA of the Enforcement Policy:

NCV 05000368/2006005-01, Fire During Hot Work Activities on the Containment Sump

Strainer.

1R07 Heat Sink Performance (71111.07)

a. Inspection Scope

The inspectors reviewed licensee programs, verified performance against industry

standards, and reviewed critical operating parameters and maintenance records for the

Unit 1 EDG A cooling water heat exchanger. The inspectors verified that:

(1) performance tests were satisfactorily conducted for heat enchanters/heat sinks and

reviewed for problems or errors; (2) the licensee utilized the periodic maintenance

method outlined in EPRI NP-7552, Heat Exchanger Performance Monitoring

Guidelines; (3) the licensee properly utilized befalling controls; (4) the licensees heat

exchanger inspections adequately assessed the state of cleanliness of their tubes; and

(5) the heat exchanger was correctly categorized under the Maintenance Rule.

  • September 5, 2006, Unit 1 EDG A cooling water heat exchanger

Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

1R08 Inservice Inspection Activities (71111.08)

Inspection Procedure 71111.08 requires four samples size as identified in

Sections 02.01, 02.02, 02.03, and 02.04.

-10- Enclosure

a. Inspection Scope

.1 Performance of Nondestructive Examination (NDE) Activities Other than Steam

Generator Tube Inspections, Pressurized Water Reactor (PWR) Vessel Upper Head

Penetration Inspections, Boric Acid Corrosion Control

The inspection procedure requires the review of NDE activities consisting of two or three

different types (i.e., volumetric, surface, or visual). The inspectors observed the

performance of three ultrasonic examinations (volumetric) (one on a section of service

water piping for wall thickness and two on field welds in the pressurizer spray line). The

inspectors also reviewed the radiographic examinations (volumetric) of the two spray

line welds. (The welds are identified in the attachment to this report.)

For each of the observed NDE activities, the inspectors verified that the examinations

were performed in accordance with the specific site procedures and the applicable

American Society of Mechanical Engineers Boiler and Pressure Vessel Code (ASME

Code) requirements.

During review of each examination, the inspectors verified that appropriate

NDE procedures were used, examinations and conditions were as specified in the

procedure, and test instrumentation or equipment was properly calibrated and within the

allowable calibration period. The inspectors also verified the NDE certifications of the

personnel who performed the above volumetric examinations. Finally, the inspectors

observed that indications identified during the radiographic examinations were

dispositioned in accordance with the ASME Code-qualified NDE procedures used to

perform the examinations.

The inspection procedure requires review of one or two examinations with recordable

indications that were accepted for continued service to ensure that the disposition was

made in accordance with the ASME Code. The inspectors were informed that no

indications exceeding ASME Code allowables were known to be in service.

The inspection procedure further requires verification of one to three welds on Class 1

or 2 pressure boundary piping to ensure that the welding process and welding

examinations were performed in accordance with the ASME Code. The inspectors

observed welding performed on a safety injection system valve in the prefabrication

shop. The inspectors verified that the welding was performed in accordance with

Sections IX and XI of the ASME Code. This included review of welding material issue

slips to establish that the appropriate welding materials had been used and verification

that the welding procedure specification (WPS E-P8-T-A8,Ar, Manual Gas Tungsten

Arc Welding (GTAW) of P-No. 8 Stainless Steels, Revision 0) had been properly

qualified.

The inspectors completed the one sample required by Section 02.01.

.2 Reactor Vessel Upper Head Penetration Inspection Activities

The inspection requirements for this section parallel the inspection requirement steps in

Section 02.01. The inspectors observed the NDEs on nine reactor vessel upper head

-11- Enclosure

penetrations. There were eight control element drive mechanism penetrations (Nos. 12,

21, 58, 59, 60, 61, 72, and 79) and one incore instrumentation penetration (No. 82).

The inspectors verified that the nondestructive activities were performed in accordance

with the requirements of NRC Order EA-03-009. The NDEs performed during the NRC

inspection did not reveal any defects or indications.

The inspectors completed the one sample required by Section 02.02.

.3 Boric Acid Corrosion Control Inspection Activities (PWRs)

The inspectors evaluated the implementation of the licensees boric acid corrosion

control program for monitoring degradation of those systems that could be deleteriously

affected by boric acid corrosion. The inspection procedure requires review of a sample

of boric acid corrosion control walkdown visual examination activities through either

direct observation or record review. The inspectors reviewed the documentation

associated with the licensees boric acid corrosion control walkdown. Additionally, the

inspectors performed independent observations of piping containing boric acid during

walkdowns of the containment building and the auxiliary building.

The inspection procedure requires verification that visual inspections emphasize

locations where boric acid leaks can cause degradation of safety significant

components. The inspectors verified through direct observation and program/record

review that the licensees boric acid corrosion control inspection efforts are directed

towards locations where boric acid leaks can cause degradation of safety-related

components.

The inspection procedure requires both a review of one to three engineering evaluations

performed for boric acid leaks found on reactor coolant system (RCS) piping and

components and one to three corrective actions performed for identified boric acid

leaks. The licensee had identified a boric acid leak on the containment spray header

during an inspection for materials that could come loose and clog the sump screens

during a loss-of-coolant accident or steam line rupture inside containment. The

inspectors reviewed the licensees analysis of the condition to evaluate the assessment

of the condition and proposed corrective actions.

The inspectors completed the one sample required by Section 02.03.

.4 Steam Generator Tube Inspection Activities

There were no steam generator tube inspections performed during this outage. The

inspectors reviewed Evaluation ER-2005-0469-001, Operational Assessment of ANO-2

Steam Generator Tubing for Cycles 18-20, dated August 31, 2006. The evaluation

concluded that no tube examinations were required to be performed during

Cycles 18-20. The inspectors noted that the basis was the condition of the tubes from

the previous inspections that were performed after the steam generators were replaced.

This sample was not completed because there was no activity to observe.

-12- Enclosure

.5 Identification and Resolution of Problems

The inspection procedure requires review of a sample of problems associated with

inservice inspections documented by the licensee in the CAP for appropriateness of the

corrective actions. The inspectors reviewed three CRs, which dealt with inservice

inspection and welding activities. From this review, the inspectors concluded that the

licensee has an appropriate threshold for entering issues into the CAP and has

procedures that direct a root cause evaluation when necessary. The licensee also had

an effective program for applying industry operating experience.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program (71111.11)

a. Inspection Scope

On December 14, 2006, the inspectors observed testing and training of Unit 1 senior

reactor operators and reactor operators to identify deficiencies and discrepancies in the

training, to assess operator performance, and to assess the evaluator's critique. The

training was a simulator training scenario.

Documents reviewed by the inspectors included:

  • ANO Unit 1 Dynamic Exam Scenario SES-1-008, Revision 5

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness (71111.12)

a. Inspection Scope

The inspectors reviewed the two below listed maintenance activities to: (1) verify the

appropriate handling of SSCs performance or condition problems; (2) verify the

appropriate handling of degraded SSC functional performance; (3) evaluate the role of

work practices and common cause problems; and (4) evaluate the handling of SSC

issues reviewed under the requirements of the Maintenance Rule, 10 CFR Part 50,

Appendix B, and TSs.

  • November 28, 2006, Unit 1, turbine building ventilation
  • December 5, 2006, Unit 2, 480-volt electrical distribution

Documents reviewed by the inspectors are listed in the attachment.

-13- Enclosure

The inspectors completed two samples.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

.1 Risk Assessment and Management of Risk

a. Inspection Scope

Risk Assessment and Management of Risk

The inspectors reviewed the six below listed assessment activities to verify:

(1) performance of risk assessments when required by 10 CFR 50.65 (a)(4) and

licensee procedures prior to changes in plant configuration for maintenance activities

and plant operations; (2) the accuracy, adequacy, and completeness of the information

considered in the risk assessment; (3) that the licensee recognizes, and/or enters as

applicable, the appropriate licensee-established risk category according to the risk

assessment results and licensee procedures; and (4) that the licensee identified and

corrected problems related to maintenance risk assessments.

  • September 19 through October 27, 2006, Unit 2, pressurizer replacement
  • September 19 through October 27, 2006, Unit 2, containment sump modification
  • November 13-17, 2006, Unit 1, planned maintenance for the week
  • November 27 through December 1, 2006, Unit 1, planned maintenance for the

week

  • December 4-8, 2006, Unit 2, planned maintenance for the week
  • December 11-15, 2006, Unit 1, planned maintenance for the week

Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed six samples.

b. Findings

No findings of significance were identified.

-14- Enclosure

1R15 Operability Evaluations (71111.15)

a. Inspection Scope

The inspectors: (1) reviewed plants status documents, such as operator shift logs,

emergent work documentation, deferred modifications, and standing orders, to

determine if an operability evaluation was warranted for degraded components;

(2) referred to the UFSAR and design basis documents to review the technical

adequacy of licensee operability evaluations; (3) evaluated compensatory measures

associated with operability evaluations; (4) determined degraded component impact on

any TSs; (5) used the significance determination process to evaluate the risk

significance of degraded or inoperable equipment; and (6) verified that the licensee has

identified and implemented appropriate corrective actions associated with degraded

components.

  • October 3, 2006, Unit 2, Electrical Bus 2B-5
  • December 19, 2006, Unit 2, containment sump

Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed four samples.

b. Findings

Introduction. A Green self-revealing noncited violation of the Unit 2 license condition for

fire protection was identified for failure of the licensee to maintain the RCP oil collection

system for RCPs C and D in an operable condition. Specifically, the licensee failed to

perform a modification on the motor installed on RCP C, which resulted in the oil

collection tank and its associated overfill berm filling up and overflowing with water from

the component cooling water (CCW) system.

Description. On September 20, 2006, while the licensee was conducting a hot

shutdown walkdown in containment during the start of Refueling Outage 2R18, the

licensee discovered that the RCP oil collection system drain tank for RCPs C and D,

(2T-110) and its associated overfill berm were filled and overflowing with water. The

licensee determined that the drain tank and associated berm were inoperable because

the licensee could not perform their intended function of providing a collection and

holding point for possible oil leakage from RCPs C and D.

The licensee obtained a sample of the water and determined that it was from the CCW

system. Based on this, the licensee then identified and performed inspections of all

interface points of the CCW system with the RCP oil collection system. During this

inspection, two leakage points were identified: the outlet flange of lube oil

Cooler 2E-25D, and the interface of the threaded supply and return piping nipples for

the lower bearing oil cooler on RCP C. The leakage from the lower bearing oil cooler

was determined to be the source that was leaking into the oil collection system through

the drip pans below the motor.

-15- Enclosure

During their investigation to determine the cause of this failure, the licensee identified

the cause of the leakage to be fatigue at the root diameter of the threaded schedule

40 pipe nipple. They also determined that this type of failure had previously occurred on

the motor installed on RCP B in December of 1995. This failure was documented in

CR ANO-2-1995-0555 and was also determined to be due to fatigue at the root diameter

of the threaded schedule 40 pipe nipple. The licensee determined, during their review

of the RCP B failure of December 1995, that Modification PEAR 9-0330, Revision 1, had

been developed and implemented to replace the schedule 40 threaded pipe nipple on

the RCPs with schedule 80 threaded pipe nipples. This modification was performed on

the motors of all installed RCPs but not the Unit 2 spare motor. Completion of the

modification on the spare RCP motor was to be accomplished during motor

refurbishment; however, the modification was never performed. In 2005 during

Refueling Outage 2R17, the spare RCP motor was installed as the RPC C motor without

the modification.

In reviewing this issue, the inspectors noted that the licensee had trend data for the

volume of oil in RCPs C and D which indicated that oil volume in RCPs C and D had

gone down over the cycle. The inspectors determined through interviews that this oil

was not contained in the oil collection system or the overflow berm as per design but

had most likely overflowed the berm and gone to the containment sump via the floor

drain system. During the operating cycle, the sump had been pumped to the auxiliary

building for processing.

Analysis. The inspectors determined that the failure to maintain the oil collection system

drain tank for RCPs C and D in an operable condition was a performance deficiency.

The finding was determined to be more than minor because it affected the protection

against external factors attribute of the mitigating systems cornerstone objective to

ensure the availability, reliability, and capability of systems that respond to initiating

events to prevent undesirable consequences. Using MC 0609, Significance

Determination Process, Phase 1 Worksheet, the finding is assumed to degrade fire

protection defense-in-depth strategies involving barriers; therefore, the significance of

the finding is determined by using Appendix F, Fire Protection Significance

Determination Process, of MC 0609. Using the Phase 1 Worksheet of Appendix F, the

inspectors assumed the condition represented a low degradation of the fire prevention

and administrative controls category since the oil collection would have kept oil from

contacting hot surfaces in the containment building. Additionally, the inspectors

assumed that no intervening combustibles were present between the overflow path and

adjacent fire areas and that the containment sump, to which the floor drains installed in

the area of the berm transported any oil that overflowed, lacked a significant ignition

source.

Enforcement. ANO Unit 2 License Condition 2.C.(3)(b), Fire Protection, states, in part,

that the licensee shall implement and maintain all provisions of the approved fire

protection program. ANO Unit 1 and Unit 2 - Fire Hazards Analysis, Revision 9, is part

of the ANO Unit 2 fire protection program. Section 6.4.5, Fire Barriers, Seals, and

Penetrations, of the Fire Hazards Analysis states, in part, that the fire barrier system at

ANO has been designed to ensure that fires will be confined or adequately retarded

from spreading to adjacent portions of the facility. Contrary to this, the filling to overflow

of the oil collection system tank and overflow berm with water from the CCW system

-16- Enclosure

during Operating Cycle 18 prevented a potential RCP oil fire in the containment

basement from being confined per the fire protection program. Because the finding is of

very low safety significance and has been entered into the licensees CAP as

CR ANO-2-2006-1407, this violation is being treated as an NCV consistent with

Section VIA of the Enforcement Policy: NCV 05000368/2006005-02, Failure to Perform

Modification Resulted in an Inoperable RCP Oil Collection System.

1R17 Permanent Plant Modifications (71111.17)

.1 Annual Review

The inspectors reviewed key affected parameters associated with energy needs,

materials/replacement components, timing, heat removal, control signals, equipment

protection from hazards, operations, flowpaths, pressure boundary, ventilation

boundary, structural, process medium properties, licensing basis, and failure modes for

the modification listed below. The inspectors verified that: (1) modification preparation,

staging, and implementation does not impair emergency/abnormal operating procedure

actions, key safety functions, or operator response to loss of key safety functions;

(2) postmodification testing maintained the plant in a safe configuration during testing by

verifying that unintended system interactions will not occur, SSC performance

characteristics still meet the design basis, the appropriateness of modification design

assumptions, and the modification test acceptance criteria has been met; and (3) the

licensee has identified and implemented appropriate corrective actions associated with

permanent plant modifications.

  • September 19 through October 26, 2006, Unit 2, pressurizer replacement

1R19 Postmaintenance Testing (71111.19)

a. Inspection Scope

The inspectors selected the six below listed postmaintenance test activities of risk

significant systems or components. For each item, the inspectors: (1) reviewed the

applicable licensing basis and/or design-basis documents to determine the safety

functions; (2) evaluated the safety functions that may have been affected by the

maintenance activity; and (3) reviewed the test procedure to ensure it adequately tested

the safety function that may have been affected. The inspectors either witnessed or

reviewed test data to verify that acceptance criteria were met, plant impacts were

evaluated, test equipment was calibrated, procedures were followed, jumpers were

properly controlled, the test data results were complete and accurate, the test

equipment was removed, the system was properly realigned, and deficiencies during

testing were documented. The inspectors also reviewed the UFSAR to determine if the

licensee identified and corrected problems related to postmaintenance testing.

  • October 17, 2006, Unit 1, Emergency Feedwater Pump P-7A
  • October 22, 2006, Unit 2, pressurizer heater capacity
  • October 24, 2006, Unit 2, replacement pressurizer relief valve monitor test

-17- Enclosure

  • October 27, 2006, Unit 2, replacement pressurizer leakage
  • November 1, 2006, Unit 2, containment building personnel hatch leakage rate

testing

Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed six samples.

b. Findings

No findings of significance were identified.

1R20 Refueling and Outage Activities (71111.20)

1. Unit 2 Forced Outage Caused by Fire in Motor Control Center 2B-53

a. Inspection Scope

The inspectors reviewed the following risk significant outage activities to verify defense

in depth commensurate with the outage risk control plan and compliance with the TSs:

(1) the risk control plan, (2) tagging/clearance activities, (3) heatup and cooldown

activities, and (4) restart activities.

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

2. Refueling and Pressurizer Replacement Outage 2R18

a. Inspection Scope

The inspectors reviewed the following risk significant refueling items or outage activities

to verify defense in depth commensurate with the outage risk control plan, compliance

with the TSs, and adherence to commitments in response to Generic Letter 88-17, Loss

of Decay Heat Removal: (1) the risk control plan, (2) tagging/clearance activities,

(3) RCS instrumentation, (4) electrical power, (5) decay heat removal, (6) spent fuel pool

cooling, (7) inventory control, (8) reactivity control, (9) containment closure, (10) reduced

inventory conditions, (11) refueling activities, (12) heatup and cooldown activities,

(13) restart activities, and (14) licensee identification and implementation of appropriate

corrective actions associated with refueling and outage activities. The inspectors

containment inspections included observation of the containment sump for damage and

debris, supports, braces, and snubbers for evidence of excessive stress, water hammer,

or aging.

-18- Enclosure

The inspectors completed one sample.

b. Findings

.1 Inadvertent RCS Draining While in Mode 5

Introduction. A Green self-revealing noncited violation of the licensees TS requirement

for procedures was identified when an operator failed to close a resin sluice header

drain valve as required by procedure. Later, while operators were aligning the unit for

alternate reactor coolant purification, a loss of approximately 230 gallons of RCS

inventory occurred.

Description. On September 14, 2006, operations personnel performed

Procedure OP-2104.019, Clean Resin Transfer, to add clean resin to Purification Ion

Exchanger 2T-36B. During this procedure, Valve 2DCH-11 was opened as part of the

system lineup. Subsequently, when the evolution was completed and the plant lineup

was being restored, station personnel failed to properly perform Step 22.2 of the

procedure leaving Valve 2DCH-11 in the open position.

Subsequently, on September 21, 2006, with Unit 2 in Mode 5, the licensee was in the

process of aligning alternate purification in accordance with Procedure OP-2104.004,

Shutdown Cooling System, Attachment J, Alternate Purification. When Step 2.11 of

this procedure was performed, the control room operators noted that pressurizer level

began to lower. The evolution was stopped and the lineup was secured. At this point,

pressurizer level stopped lowering. Station personnel performed a system walkdown

and discovered that Valve 2DCH-11 was in the open position. Operations personnel

determined that approximately 230 gallons were drained from the RCS through the open

valve.

During their review, the inspectors noted that Procedure OP-2104.004, Attachment J,

directed personnel to prepare a caution tag for components to prevent the loss of RCS

inventory. However, the procedure contained a note that preceded Step 1.11 which

directed the caution tag be hung on the room door instead of Valve 2DCH-11 and two

other valves. This tag stated that, since the valves were normally closed, any

misalignment would be detected by system abnormalities. The inspectors determined

that this note contributed to Valve 2DCH-11 not being discovered out of position prior to

initiating alternate purification since the licensee did not perform a valve lineup

verification.

Analysis. The failure of station personnel to manipulate Valve 2DCH-11 in accordance

with station procedure was determined to be a performance deficiency. The finding was

determined to be more than minor because it affected the configuration control attribute

of the initiating events cornerstone objective to limit the likelihood of those events that

upset plant stability and challenge critical safety functions during shutdown as well as

power operations. The inspectors used MC 0609, Significance Determination Process,

Appendix G, Shutdown Operations Significance Determination Process, and assumed

that the administrative controls implemented to avoid operations that could lead to

perturbations in RCS level control attribute was affected. The finding was determined to

have very low safety significance because the finding did not result in a loss of 2 feet or

-19- Enclosure

more of RCS inventory and did not result in a loss of RCS inventory while the unit was in

reduced inventory. The cause of the finding is related to the crosscutting aspect of

human performance associated with work practices because the operator failed to use

error prevention techniques like self checking and peer checking which would have

prevented the event.

Enforcement. Unit 2 TS, Section 6.4.1.a, Procedures, requires, in part, that written

procedures shall be established, implemented, and maintained covering the applicable

procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A,

February 1978. Procedure OP-2104.019, Clean Resin Transfer, is a procedure

required by Regulatory Guide 1.33. Contrary to the above, on September 14, 2006, the

licensee failed to fully implement Procedure OP-2104.019, Clean Resin Transfer,

when the licensee failed to close Valve 2DCH-11. Because this finding is of very low

safety significance and has been entered into the CAP as CR ANO-2-2006-1464, this

violation is being treated as an NCV, consistent with Section VIA of the NRC

Enforcement Policy: NCV 05000368/2006005-03, Inadvertent RCS Draining While in

Mode 5.

.2 Unplanned Increase in Time with Reactor Vessel Water Level at Flange Level

Introduction. A Green self-revealing finding was identified associated with the licensees

use of a hammer to remove and reinstall both the main hook pin and the load cell pin on

the Unit 2 polar crane. Unit 2 was maintained in a condition with reactor vessel water

level being maintained just below the reactor vessel flange for an additional unplanned

27 hours3.125e-4 days <br />0.0075 hours <br />4.464286e-5 weeks <br />1.02735e-5 months <br /> when the pins could not be used due to deformation by the hammer.

Description. On September 24, 2006, station personnel were preparing the Unit 2 polar

crane for the reactor vessel closure head removal. This involved removing the normally

installed main hook, installing a load cell, and then reinstalling the main hook. During

performance of Procedure OP-2504.005, Reactor Vessel Closure Head Removal,

Revision 12, Step 7.22, licensee personnel were unable to easily remove the polar crane

main hook pin. After the pin was removed, it was examined by the licensee and

discovered to be mushroomed at one end. When the licensee inspected the pin used to

secure the load cell into place, it was discovered to be in the same condition. The

licensee determined this condition to be caused by the practice of using a hammer, as

necessary, to both remove and install the pins during previous refueling outages.

The inspectors noted that the licensee did not have a formal procedure that controlled

the removal and installation of the pins, and that station personnel were controlling this

evolution as a skill-of-the-craft process. A review of the applicable procedures by the

inspectors revealed that Procedure OP-2504.005, Step 7.22, Reactor Vessel Closure

Head Removal, simply states, Verify that the load cell is attached to the polar crane.

The inspectors also determined that the use of hammers was a common practice being

used to remove and reinstall the pins on the polar crane, and there was no existing

evaluation for the effects of this on the integrity of the pins. The inspectors determined

that the lack of adequate procedural direction and the practice of hammering the pins in

and out directly contributed to the deformation of the pins. Finally, the inspectors were

informed by licensee personnel that the practice of using hammers to remove the pins

-20- Enclosure

was not part of the formal training received by maintenance personnel; however, in at

least one instance, a discussion between instructors and maintenance personnel

outside the formal lesson plan had occurred describing the practice of using hammers

as being acceptable.

Analysis. The inspectors determined that the licensees failure to provide clear guidance

and training on how to remove the main hook and load cell pins without causing damage

was a performance deficiency. The finding was determined to be more than minor

because it affected the equipment performance attribute of the initiating events

cornerstone objective to limit the likelihood of those events that upset plant stability and

challenge critical safety functions during shutdown as well as power operations. The

inspectors evaluated the finding using MC 0609, Significance Determination Process,

Appendix G, Shutdown Operations Significance Determination Process. The

inspectors determined that the finding was not a loss of shutdown control as defined by

MC 0609, Appendix G, Table 1, and then evaluated the issue using Checklist 3 of

MC 0609, Appendix G, Attachment 1. The inspectors determined that a quantitative

analysis was not required because the event did not represent a reduction in mitigation

capability which would have increased the frequency of occurrence of a loss of decay

heat removal. Therefore, the finding was determined to have very low safety

significance. The cause of the finding is related to the crosscutting element of human

performance associated with resources because the training of personnel and

procedural guidance available was adequate.

Enforcement. While a performance deficiency was identified, there were no violations of

NRC requirements identified during the review of this issue. The licensee has entered

this issue into the CAP as CR ANO-2-2006-1553: Finding (FIN)05000368/2006005-04,

Unplanned Increase in Time with Reactor Vessel Water Level at Flange Level.

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors reviewed the UFSAR, procedure requirements, and TSs to ensure that

the four below listed surveillance activities demonstrated that the SSCs tested were

capable of performing their intended safety functions. The inspectors either witnessed

or reviewed test data to verify that the following significant surveillance test attributes

were adequate: (1) preconditioning; (2) evaluation of testing impact on the plant;

(3) acceptance criteria; (4) test equipment; (5) procedures; (6) jumper/lifted lead

controls; (7) test data; (8) testing frequency and method demonstrated TS operability;

(9) test equipment removal; (10) restoration of plant systems; (11) fulfillment of ASME

Code requirements; (12) updating of performance indicator (PI) data; (13) engineering

evaluations, root causes, and bases for returning tested SSCs not meeting the test

acceptance criteria were correct; (14) reference setting data; and (15) annunciators and

alarms setpoints. The inspectors also verified that the licensee identified and

implemented any needed corrective actions associated with the surveillance testing.

  • August 4, 2006, Unit 1, makeup system Valve MU-36A local leak rate test
  • October 15, 2006, Unit 2, Valve 2SV-8271-2 local leak rate test

-21- Enclosure

  • October 23, 2006, Unit 2, Containment Cooler A

Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed four samples.

b. Findings

No findings of significance were identified.

Cornerstone: Emergency Preparedness

1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)

a. Inspection Scope

The inspector performed an in-office review of Revision 037-05-0 to Emergency Plan

Implementing Procedure OP-1903.010, Emergency Action Level Classification. The

revision was submitted in October 2006. The revision corrected emergency plan

guidance for transient event classification and notification practices at Arkansas Nuclear

One and was a corrective action for the NCV 05000313,368/2006003-02, Failure to

Meet Immediate Notification Requirements during Transient Events.

The revision was compared to the previous revision, to the criteria of NUREG-0654,

Criteria for Preparation and Evaluation of Radiological Emergency Response Plans and

Preparedness in Support of Nuclear Power Plants, Revision 1; and NEI 99-01,

Methodology for Development of Emergency Action Levels, Revision 2; and to the

standards in 10 CFR 50.47(b) to determine if the revision was adequately conducted

following the requirements of 10 CFR 50.54(q). This review was not documented in a

safety evaluation report and did not constitute approval of licensee changes, therefore,

the revision is subject to future inspection.

The inspector completed one sample during the inspection.

b. Findings

No findings of significance were identified.

1EP6 Drill Evaluation (71114.06)

a. Inspection Scope

For the one below listed simulator-based training evolutions contributing to drill/exercise

performance, emergency response organization, and PIs, the inspectors: (1) observed

the training evolution to identify any weaknesses and deficiencies in classification,

notification, and protective action requirements (PAR) development activities;

(2) compared the identified weaknesses and deficiencies against licensee identified

-22- Enclosure

findings to determine whether the licensee is properly identifying failures;

and (3) determined whether licensee performance is in accordance with the guidance of

the NEI 99-02, Voluntary Submission of Performance Indicator Data, acceptance

criteria.

  • December 7, 2006, Unit 2, simulator-based exercise requiring notice of unusual

event and alert declarations

Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

2. RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2OS1 Access Control To Radiologically Significant Areas (71121.01)

a. Inspection Scope

This area was inspected to assess the licensees performance in implementing physical

and administrative controls for airborne radioactivity areas, radiation areas, high

radiation areas, and worker adherence to these controls. The inspectors used the

requirements in 10 CFR Part 20, the TSs, and the licensees procedures required by

TSs as criteria for determining compliance. During the inspection, the inspectors

interviewed the radiation protection manager, radiation protection supervisors, and

radiation workers. The inspectors performed independent radiation dose rate

measurements and reviewed the following items:

  • PI events and associated documentation packages reported by the licensee in

the occupational radiation safety cornerstone

  • Controls (surveys, posting, and barricades) of radiation, high radiation, or

airborne radioactivity areas

  • Radiation work permits, procedures, engineering controls, and air sampler

locations

  • Conformity of electronic personal dosimeter alarm set points with survey

indications and plant policy; workers knowledge of required actions when their

electronic personnel dosimeter noticeably malfunctions or alarms

areas

  • Adequacy of the licensees internal dose assessment for any actual internal

exposure greater than 50 millirem committed effective dose equivalent

-23- Enclosure

  • Physical and programmatic controls for highly activated or contaminated

materials (nonfuel) stored within spent fuel and other storage pools

  • Self-assessments related to the access control program since the last

inspection; there were no audits, licensee event reports, and special reports

documented.

  • Corrective action documents related to access controls
  • Licensee actions in cases of repetitive deficiencies or significant individual

deficiencies

  • Radiation work permit briefings and worker instructions
  • Adequacy of radiological controls such as, required surveys, radiation protection

job coverage, and contamination controls during job performance

  • Dosimetry placement in high radiation work areas with significant dose rate

gradients

and very high radiation areas

  • Controls for special areas that have the potential to become very high radiation

areas during certain plant operations

  • Posting and locking of entrances to all accessible high dose rate - high radiation

areas and very high radiation areas

  • Radiation worker and radiation protection technician performance with respect to

radiation protection work requirements

The inspectors completed 21 of the required 21 samples.

b. Findings

No findings of significance were identified.

4. OTHER ACTIVITIES

4OA1 PI Verification (71151)

.1 Occupational Radiation Safety Cornerstone

a. Inspection Scope

The inspectors reviewed licensee documents from April through September 2006. The

review included corrective action documentation that identified occurrences in locked high

radiation areas (as defined in the licensees TSs, very high radiation areas (as defined in

10 CFR 20.1003), and unplanned personnel exposures (as defined in NEI 99-02).

Additional records reviewed included as low as reasonably achievable records and whole

body counts of selected individual exposures. The inspectors interviewed licensee

-24- Enclosure

personnel that were accountable for collecting and evaluating the PI data. In addition, the

inspector toured plant areas to verify that high radiation, locked high radiation, and very

high radiation areas were properly controlled. PI definitions and guidance contained in

NEI 99-02, Regulatory Assessment Indicator Guideline, Revision 4, were used to verify

the basis in reporting for each data element.

  • Occupational Exposure Control Effectiveness

The inspectors completed the required sample (1) in this cornerstone

b. Findings

No findings of significance were identified.

.2 Public Radiation Safety Cornerstone

a. Inspection Scope

The inspectors reviewed licensee documents from April through September 2006.

Licensee records reviewed included corrective action documentation that identified

occurrences for liquid or gaseous effluent releases that exceeded PI thresholds and those

reported to the NRC. The inspectors interviewed licensee personnel that were

accountable for collecting and evaluating the PI data. PI definitions and guidance

contained in NEI 99-02, Regulatory Assessment Indicator Guideline, Revision 4, were

used to verify the basis in reporting for each data element.

  • Radiological Effluent TS/Offsite Dose Calculation Manual Radiological Effluent

Occurrences

The inspectors completed the required sample (1) in this cornerstone

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems (71152)

.1 Routine Review of Identification and Resolution of Problems

The inspectors performed a daily screening of items entered into the licensees CAP.

This assessment was accomplished by reviewing CRs and attending corrective action

review and work control meetings. The inspectors: (1) verified that equipment, human

performance, and program issues were being identified by the licensee at an appropriate

threshold and that the issues were entered into the CAP; (2) verified that corrective

actions were commensurate with the significance of the issue; and (3) identified conditions

that might warrant additional follow-up through other baseline inspection procedures.

.2 Selected Issue Follow-up Inspection

In addition to the routine review, the inspectors selected the two below listed issues for a

more in-depth review. The inspectors considered the following during the review of the

licensees actions: (1) complete and accurate identification of the problem in a timely

-25- Enclosure

manner; (2) evaluation and disposition of operability/reportability issues; (3) consideration

of extent of condition, generic implications, common cause, and previous occurrences;

(4) classification and prioritization of the resolution of the problem; (5) identification of root

and contributing causes of the problem; (6) identification of corrective actions;

and (7) completion of corrective actions in a timely manner.

  • September 20, 2006, Unit 2, repeat occurrence of containment purge isolation
  • October 30, 2006, Unit 2, repeat occurrence of improper electrical connections in

motor-control centers

When evaluating the effectiveness of the licensees corrective actions for these issues,

the following attributes were considered:

  • Complete and accurate identification of the problem in a timely manner

commensurate with its significance and ease of discovery

  • Evaluation and disposition of operability and reportability issues
  • Consideration of extent of condition, generic implications, common cause, and

previous occurrences

  • Classification and prioritization of the resolution of the problem commensurate with

its safety significance

  • Identification of root and contributing causes of the problem for significant

conditions adverse to quality

  • Identification of corrective actions which are appropriately focused to correct the

problem

  • Completion of corrective actions in a timely manner commensurate with the safety

significance of the issue

Documents reviewed by the inspectors are listed in the attachment

.3 Semiannual Trend Review

a. Inspection Scope

The inspectors completed a semi-annual trend review of repetitive or closely related

issues that were documented in corrective action documents to identify trends that might

indicate the existence of more safety-significant issues. The inspectors' review consisted

of the 6-month period of June 24 through December 31, 2006. When warranted, some of

the samples expanded beyond those dates to fully assess the issue. The inspectors also

reviewed CAP items associated with deficiencies in the conduct of activities involving hot

work. The inspectors compared and contrasted their results with the results contained in

the licensees quarterly trend reports. Corrective actions associated with a sample of the

issues identified in the licensees trend report were reviewed for adequacy. Documents

reviewed by the inspectors are listed in the attachment.

-26- Enclosure

b. Findings

During the Unit 2 pressurizer replacement Refueling Outage 2R18 from September 19

through October 28, 2006, several deficiencies were noted involving the conduct of hot

work. Licensee Procedure EN-DC-127, Control of Hot Work and Ignition Sources,

contains the governing guidelines for the conduct of hot work, including Hot Work

Permit, Attachment 8.1, which serves to document that the applicable requirements for

each activity involving hot work are met. Examples of instances resulting from failures to

adequately implement the control of hot work procedure included:

  • On September 24, 2006, welding activities being conducted on the Unit 2 main

condenser manway cover resulted in paint/crud smoldering that was extinguished

with a portable fire extinguisher.

  • On September 25, 2006, sparks from torch cutting of the Unit 2 containment sump

strainer ignited a nearby plastic bag containing used anti-contamination clothing.

  • On September 26, 2006, a substantial amount of slag from the containment sump

strainer torch cutting flowed down onto a fire blanket that was protecting the floor

and caused the fire blanket to ignite.

  • On September 27, 2006, slag from the containment sump strainer torch cutting

flowed down through a fire blanket and landed on Valve 2BS-38 in the containment

sump. The slag came in contact with debris buildup on the valve locking chain and

began to smoke and smolder. A portable fire extinguisher was discharged to

extinguish the smoldering.

  • On September 28, 2006, the firewatch posted for the containment sump strainer

hot work could not get to his designated fire extinguisher. The firewatch had

moved to the east side of the sump and the extinguisher remained on the west

side of the sump.

  • On October 5, 2006, a small fire in the Unit 2 containment building basement

below the pressurizer was extinguished by the assigned firewatch using a portable

extinguisher.

  • On October 16, 2006, welding and grinding activities above the replacement

pressurizer were being performed without proper protection to prevent sparks from

traveling down the cavity below.

The licensee entered each of these occurrences into their CAP.

.4 Access Control to Radiologically Significant Areas

Section 2OS1 evaluated the effectiveness of the licensee's problem identification and

resolution processes regarding access controls to radiologically significant areas and

radiation worker practices. The inspectors reviewed corrective action documents for root

cause/apparent cause analysis against the licensees problem identification and resolution

process. No findings of significance were identified.

-27- Enclosure

4OA3 Follow-up of Events and Notices of Enforcement Discretion (71153)

a. Inspection Scope

The inspectors: (1) reviewed operator logs, plant computer data, and/or strip charts for

the below listed evolutions to evaluate operator performance in coping with nonroutine

events and transients; (2) verified that operator actions were in accordance with the

response required by plant procedures and training; and (3) verified that the licensee has

identified and implemented appropriate corrective actions associated with personnel

performance problems that occurred during the nonroutine evolutions sampled.

  • October 30, 2006, Unit 2, fire in Motor-Control Center 2B-53
  • November 9, 2006, Unit 1, unplanned loss of Main Feedwater Pump P-2A

Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed three samples.

b. Findings

Introduction. A Green self-revealing finding was identified when the licensee replaced an

air conditioning unit for the Unit 1 Main Feedwater Pump (MFP) A control cabinet without

considering the effects of electromagnetic interference (EMI) on the digital speed

monitor (DSM) housed in the cabinet. Consequently, MFP A tripped, resulting in an

unplanned automatic plant power reduction from 100 percent to 40 percent RTP.

Description. In September 2006 the air conditioning unit for the Unit 1 MFP A cabinet

failed. During the procurement phase of replacement efforts, the station discovered that

the current air conditioning unit was no longer available because it had become obsolete.

The licensee contacted the cabinet manufacturer who recommended to the licensee a

replacement unit. On October 12 the licensee replaced the air conditioning unit with the

recommended replacement after evaluating it as being an equivalent unit in accordance

with Procedure EN-DC-313, Procurement Engineering Process, Revision 0.

Subsequently, on November 9, 2006, while Unit 1 was operating at 100 percent RTP

MFP A tripped, which caused the integrated control system to initiate and perform an

unplanned automatic power reduction to 40 percent RTP. Operators surveyed the

indications and concluded that the cause of the MFP trip was an overspeed condition;

however, at the time of the trip, there were no indications that the MFP had actually

experienced an overspeed.

After extensive troubleshooting, the licensee suspected that EMI from the air conditioning

unit was the cause of the faults. The licensee performed a review of the new air

conditioning unit and identified that the bottom section of the new unit was molded plastic

and not metal like the previous unit. They also discovered the configuration of this new

unit placed the blower fan directly above, and in closer proximity to, the DSM than did that

of the previous air conditioning unit. The licensee decided to remove power to the air

conditioning unit to verify that it was the initiator of the faults in the DSM. With power to

the air conditioning unit removed, the faults and trips did not recur.

-28- Enclosure

The inspectors reviewed the licensees root cause evaluation of this event, documented in

CR ANO-1-2006-1399, which determined the root cause to be that the procurement

engineering equivalency guidelines did not consider EMI as a potential failure mode.

During this review, the inspectors noted that the licensee had not questioned or

investigated any of the differences between the old and the new air conditioning units.

Instead, the licensee had relied on the manufacturers designation that the new unit was

an equivalent replacement for the old unit.

Also, during their review of the root cause analysis, the inspectors noted that there had

been previous experiences with the MFP A control system involving EMI, as well as a

substantial amount of industry operating experience concerning the topic of EMI and

digital components. During interviews with station personnel, the inspectors also

determined that station engineers received specific training on EMI related to digital

components.

Analysis. The inspectors determined that the failure of the licensee to adequately

evaluate the new air conditioning unit with respect to design differences and possible

EMI interactions was a performance deficiency. The finding was determined to be more

than minor because it affected the design control attribute of the initiating events

cornerstone objective to limit the likelihood of those events that upset plant stability and

challenge critical safety functions during shutdown as well as power operations. Using the

MC 0609, Significance Determination Process, Phase 1 Worksheet, the finding is

determined to have very low safety significance because the condition only affected the

initiating events cornerstone and did not contribute to both the likelihood of a reactor trip

and the likelihood that mitigation equipment or functions will not be available. The cause

of the finding is related to the crosscutting element of problem identification and resolution

associated with operating experience because the licensees failure to implement and

institutionalize OE through changes to station processes and procedures.

Enforcement. While a performance deficiency was identified with regard to the trip of the

MFP A, there were no violations identified during the review of this issue. The licensee

has entered this issue into the CAP as CR ANO-1-2006-1399: FIN 05000313/2006005-5,

Trip of a MFP Due to Inadequate Design Control.

4OA5 Other Activities

.1 (Closed) Temporary Instruction (TI) 2515/169, Mitigating Systems Performance

Index (MSPI) Verification

a. Inspection Scope

During this inspection period, the inspectors completed a review of the licensees

implementation of the MSPI in accordance with the guidance provided in TI 2515/169.

The review examined the licensees MSPI Basis Documents (ANO1-A-6-0001, Revision 1,

and ANO2-SA-06-00001, Revision 0) and verified the established system boundaries and

monitored components were consistent with guidance provided in NEI 99-02, Reactor

Oversight Process Performance Indicators, Revision 4. The inspectors verified that the

licensee did not include credit for unavailability hours for short term unavailability or

operator recovery actions to restore the risk-significant function as is allowed by

NEI 99-02.

-29- Enclosure

Additionally, the inspectors reviewed the baseline MSPI unavailability time using plant

specific values for the period of 2002 through 2004. The verification included all planned

and unplanned unavailability. For Unit 1, the inspectors reviewed the baseline MSPI

unreliability data using plant specific values for the period of 2002 through 2004. Unit 2

derived its baseline unreliability on industry standard values, as is permitted by NEI 99-02.

The plant specific data for 2005 through 2006 were also reviewed to ensure the licensee

properly accounted for the actual unavailability hours of MSPI systems. For the same

period, the MSPI component unreliability data was examined to ensure the licensee

identified all failures of monitored components. The accuracy and completeness of the

reported unavailability and unreliability data was verified by reviewing operating logs, CRs,

and work order documents. The unavailability and unreliability data was compared with PI

data submitted to the NRC to ensure that any discrepancies would not result in a change

to the index color.

b. Findings

No findings of significance were identified. This completes the inspection requirements

for this TI.

.2 Institute of Nuclear Power Operations Plant Assessment Report Review

a. Inspection Scope

The inspectors reviewed the final report for the Institute of Nuclear Power Operations

plant assessment of Arkansas Nuclear One, Units 1 and 2, conducted in July and

August 2006. The inspectors reviewed the report to ensure that issues identified were

consistent with the NRC perspectives of licensee performance and to verify if any

significant safety issues were identified that required further NRC followup.

b. Findings

No findings of significance were identified.

.3 (Closed) Unresolved Item (URI)05000313/2006003-01, Failure to Retrieve Required

Records of Activities Affecting Quality

In response to inspectors questioning the seismic capability of the Tendon Surveillance

Cranes L-28 on Unit 1, the licensee could not locate the appropriate documentation. The

licensee evaluated the as found conditions of the cranes against the uniformed building

code. The licensee concluded that the cranes would be able to withstand the design

basis earthquake without affecting mitigating equipment. These evaluations were

reviewed by the inspectors. No findings of significance were identified, and no violations

of NRC requirements were identified. The licensee documented the evaluations

demonstrating the seismic qualification in CR ANO-1-2005-3109. This unresolved

item (URI) is closed.

-30- Enclosure

.4 NRC TI 2515/166, PWR Containment Sump Blockage

The inspectors reviewed ANOs Unit 2 implementation of plant modifications and

procedure changes committed to in their response to Generic Letter 2004-02, Potential

Impact of Debris on Emergency Recirculation During Design Basis Accidents at

Pressurized Water Reactors.

The inspectors observed installation of the containment recirculation sump strainers,

debris barriers, and interceptors. In addition, the inspectors verified that ANO Unit 2 has

implemented specific procedure changes to control tags, labels, tape, and other objects

inside the containment building.

At the time of the inspection, industry testing for chemical effects on containment

recirculation sumps was not complete. Since the testing was not complete, ANO Unit 2

evaluated the new recirculation sump modifications to the original design basis,

Regulatory Guide 1.82, Water Sources for Long-Term Recirculation Cooling Following a

Loss-of-Coolant Accident, Revision 0. Final review and acceptance of the modification

will be performed by the Office of Nuclear Reactor Regulation at a later date.

4OA6 Meetings, Including Exit

On October 6, 2006, the inspectors presented the access controls inspection results to

Mr. T. Mitchell, General Manager and other members of his staff who acknowledged the

findings. The inspectors confirmed that proprietary information was not provided or

examined during the inspection.

The engineering inspectors presented the results of the inservice inspection review to

Mr. J. Kowalewski, Director, Engineering, on October 10, 2006. Mr. Kowalewski

acknowledged the inspection findings. The engineering inspector conducted a followup

exit with Mr. T. Mitchell, General Manager, Plant Operations, on December 4, 2006, to

provide updated information on the documentation associated with the review of the

containment sump modification. The inspectors identified that they had not reviewed

proprietary information.

On November 1, 2006, the inspector presented the results of the emergency plan change

inspection to Mr. R. Holeyfield, Supervisor, Emergency Preparedness. The inspector

confirmed that proprietary information was not provided or examined during the

inspection.

The resident inspectors presented the inspection results of the resident inspections to

Mr. J. Forbes, Vice President, Operations, and other members of the licensee's

management staff on January 17, 2007. The resident inspectors conducted a followup

exit with Mr. J. Forbes, Vice President, Operations, on February 8, 2007. The licensee

acknowledged the findings presented. The inspectors noted that while proprietary

information was reviewed, none would be included in this report.

ATTACHMENT: SUPPLEMENTAL INFORMATION

-31- Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

R. Barnes, Manager, Planning, Scheduling, and Outages

S. Bennett, Project Manager, Licensing

B. Berryman, Manager, Operations Unit 1

J. Browning, Manager, Operations Unit 2

S. Cotton, Manager, Training

B. Daiber, Supervisor, Systems Engineering

J. Eichenberger, Manager, Corrective Actions and Assessments

J. Forbes, Vice President, Operations

R. Fowler, Emergency Planner

R. Freeman, Emergency Planner

J. Giles, Manager, Technical Support

M. Ginsberg, Supervisor, Engineering Programs and Components

R. Gresham, Emergency Planner

D. Harris, Emergency Planner

A. Hawkins, Licensing Specialist

J. Hoffpauir, Manager, Maintenance

R. Holeyfield, Manager, Emergency Planning

M. Huff, Supervisor, Project Engineering

D. James, Manager, Licensing

W. James, Manager, Engineering Projects

J. Kowalewski, Director, Engineering

T. Marlow, Director, Nuclear Safety Assurance

J. Miller, Jr., Manager, System Engineering

T. Mitchell, General Manager, Plant Operations

D. Moore, Manager, Radiation Protection

K. Panther, Nondestructive Examination Site Level III

C. Reasoner, Manager, Engineering Programs and Components

C. Tyrone, Manager, Quality Assurance

F. Van Buskirk, Licensing Specialist

D. White, Emergency Planner

P. Williams, Supervisor, Systems Engineering

M. Woodby, Manager, Design Engineering

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000368/2006005-01 NCV Fire During Hot Work Activities on the Containment Sump

Strainer (Section 1R05)05000368/2006005-02 NCV Failure to Perform Modification Resulted in an Inoperable

RCP Oil Collection System (Section 1R15)

A-1 Attachment

05000368/2006005-03 NCV Inadvertent RCS Draining While in Mode 5 (Section 1R20)05000368/2006005-04 FIN Unplanned Increase in Time with Reactor Vessel Water Level

at Flange Level (Section 1R20)05000313/2006005-05 FIN Trip of a MFP Due to Inadequate Design Control

(Section 4OA3)

Closed

05000313/2006003-01 URI Failure to Retrieve Required Records of Activities Affecting

Quality (Section 4OA5)

Discussed

None

LIST OF DOCUMENTS REVIEWED

In addition to the documents referred to in the inspection report, the following documents were

selected and reviewed by the inspectors to accomplish the objectives and scope of the inspection

and to support any findings:

Section 1R01: Adverse Weather Protection

NUMBER TITLE REVISION

OP-2203.008 Natural Emergencies 9

OP-1203.025 Natural Emergencies 20

Section 1R02: Evaluation of Changes, Tests, or Experiments

Engineering Requests

NUMBER TITLE REVISION

ER-ANO-2002-0836-003 Pressurizer Replacement 1

ER-ANO-2002-0836-004 Original Pressurizer Removal / Replacement 1

Pressurizer Installation

ER-ANO-2002-0836-020 Replacement Pressurizer Heater Electrical Design 0

Input

A-2 Attachment

Section 1R04: Equipment Alignment

Procedures

NUMBER TITLE REVISION

OP-1104.036 Emergency Diesel Generator Operations 45

Op-1107.002 ES Electrical System Operations 23

OP-1104.005 Reactor Building Spray System Operation 46

Section 1R05: Fire Protection

Plant Drawings

FZ-1038, Sheet 1, Revision 2

FZ-2018, Sheet 1, Revision 2

Procedures

NUMBER TITLE REVISION

Arkansas Nuclear One Fire Hazards Analysis 11

PFP-U1 ANO Prefire Plan (Unit 1) - Section 1B-357-67-U.doc, 2

Section 1B-354-79-U.doc

PFP-U2 ANO Prefire Plan (Unit 2) - Section 2B-335-2040- 2

JJ.doc

EN-DC-127 Control of Hot Work and Ignition Sources 2

CRs

ANO-1-2005-0950 ANO-2-2005-1724 ANO-2-2006-1565 ANO-2-2006-1701

ANO-1-2005-1397

Section 1R07: Heat Sink Performance

NUMBER TITLE REVISION

ULD-1-SYS-01 ANO-1 Emergency Diesel Generator (EDG) System 4

ULD-1-SYS-10 ANO-1 Service Water Systems 13

SPEC-6600-M-012 Emergency Diesel Generators for ANO Unit 1 1

ER-ANO-2004-0663-000 2004 Unit 1 EDG Thermal Test Results 0

ER-980310 EDG Coolers, E-20A/B, Service Water Flow

Requirements

CALC-91-R-2013-01 Service Water Performance Testing Methodology 14

A-3 Attachment

OP-1309.018 EDG Cooler Thermal Test Change 004-02-0

Section 1R08: Inservice Inspection (71111.08P)

CRs:

ANO-2-2005-0916 ANO-2-2006-1208 ANO-C-2006-1733

NDEs

REPORT COMPONENT/LOCATION METHOD

BOP-RT-06-055 FW-50 (WDR-40631) Drawing No. 2CCA-15-1, Sheet 1 Radiographic

BOP-RT-06-056 FW-51 (WDR-40632) Drawing No. 2CCA-15-1, Sheet 1 Radiographic

ISI-UT-06-033 2-73-SWS-R-12B-30R, 2HBC-60-1 between FW-52C & Automatic

FW-6C1 Ultrasonic

ISI-UT-06-040 FW-50 (WDR-40631) Drawing No. 2CCA-15-1, Sheet 1 Ultrasonic

ISI-UT-06-042 FW-51 (WDR-40632) Drawing No. 2CCA-15-1, Sheet 1 Ultrasonic

Procedures

PROCEDURE TITLE REVISION

CEP-NDE-0110 Program Section for Certification of NDE Personnel 2

CEP-NDE-0111 Certification of Ultrasonic Personnel in Accordance 1

with ASME Section XI, Appendix VII

CEP-NDE-0400 Ultrasonic Examination 0

CEP-NDE-0404 Manual Ultrasonic Examination of Ferritic Piping 1

Welds (ASME XI)

CEP-NDE-0423 Manual Ultrasonic Examination of Austenitic Piping 1

Welds (ASME XI)

CEP-NDE-0505 Ultrasonic Thickness Examination 3

A-4 Attachment

Welding Procedures/Qualification Records

NUMBER TITLE REVISION/

DATE

PQR 107 Manual Gas Tungsten & Shielded Metal Arc 1

Welding (GTAW & SMAW), P-No. 8, SA-312 Type

304

PQR 170 Manual Gas Tungsten & Shielded Metal Arc 1

Welding (GTAW & SMAW), P-No. 8, SA-240 Type

304

WPS E-P8-T-A8,Ar Manual Gas Tungsten Arc Welding (GTAW) of 0

P-No. 8 Stainless Steels

WPS E-P8-T(M)-A8,Ar Machine Gas Tungsten Arc Welding (GTAW) of 0

P-No. 8 Stainless Steels

WP 06-121 2T-1 Surge Line October 3,

2006

Section 1R13: Maintenance Risk Assessments and Emergent Work Control

COPD-024, Risk Assessment Guidelines, Revision 18

Section 1R15: Operability Evaluations

CRs

ANO-2-1995-0555 ANO-2-2006-1459 ANO-2-2006-1522 ANO-2-2006-1796

ANO-2-2006-1407 ANO-2-2006-1478 ANO-2-2006-1539 ANO-2-2006-1853

ANO-2-2006-1433 ANO-2-2006-1521 ANO-2-2006-1757 ANO-2-2006-1879

Procedure

OP-2305.002, Reactor Coolant System Leak Detection, Revision 14

Engineering Requests

ER-ANO-2000-2528-003, ANO Sump Operability when the RCS Temperature is Above 200 F

ER-ANO-2004-0060-000, ANO-2 Sump Operability for the RCS Temperature above 200 F

Miscellaneous Documents

2CNA108802, Safety Evaluation Report, dated October 26, 1988

0CAN088404, Station Letter to USNRC Requesting Exemption, dated August 15, 1984

A-5 Attachment

Section 1R17: Permanent Plant Modifications

Engineering Requests

NUMBER TITLE

ER-ANO-2002-0836-003 Pressurizer Replacement

ER-ANO-2002-0836-004 Original Pressurizer Removal / Replacement

Pressurizer Installation

ER-ANO-2002-0836-005 Interference Removal / Reinstallation Inside the

Pressurizer Cubicle

ER-ANO-2002-0836-006 Interference Removal / Reinstallation Outside the

Pressurizer Cubicle

ER-ANO-2002-0836-007 ANO-2 Pressurizer Replacement Rigging and

Handling

ER-ANO-2002-0836-020 Replacement Pressurizer Heater Electrical Design

Input

Section 1R20: Refueling and Outage Activities

Procedures

NUMBER TITLE REVISION

OP-2104.004 Shutdown Cooling System 031-00-0

OP-2104.019 Clean Resin Transfer 009-01-0

OP-2504.005 Reactor Vessel Closure Head Removal 012-01-0

Miscellaneous Document

Shutdown Operations Protection Plan, dated August 4, 2005

CRs

ANO-2-2006-1464 ANO-2-2006-1573 ANO-2-2006-2032 ANO-C-2006-1678

ANO-2-2006-1553 ANO-2-2006-1734 ANO-C-2006-1473

Section 2OS1: Access Controls to Radiologically Significant Areas

CRs

ANO-1-2006-0479 ANO-2-2006-1434 ANO-2-2006-1497 ANO-2-2006-1568

ANO-1-2006-0700 ANO-2-2006-1446 ANO-2-2006-1501 ANO-2-2006-1568

ANO-1-2006-1113 ANO-2-2006-1471 ANO-2-2006-1511 ANO-2-2006-1575

ANO-2-2005-1429 ANO-2-2006-1495 ANO-2-2006-1523 ANO-2-2006-1598

A-6 Attachment

ANO-2-2006-1606 ANO-2-2006-1674 ANO-2-2006-1716 ANO-2-2006-1774

ANO-2-2006-1636 ANO-2-2006-1675 ANO-2-2006-1717 ANO-2-2006-1790

ANO-2-2006-1638 ANO-2-2006-1695 ANO-2-2006-1748 ANO-C-2006-1698

ANO-2-2006-1671 ANO-2-2006-1696 ANO-2-2006-1765

Audits and Self-Assessments

Self-Assessment Report, QS-2006-ANO-007, 2R18 Radiation Protection Outage Planning

Review

Radiation Work Permits

NUMBER TITLE

RWP 2006-2420 Scaffold Activities

RWP 2006-2501 Support Activities for Pressurizer Replacement

RWP 2006-2502 Remove and Replace Pressurizer

RWP 2006-2520 Incore Instrument Thimble Tube Replacement

RWP 2005-2530 Sump Screen Modification

RWP 2006-2540 Hot Leg RTD Replacement

Procedures

NUMBER TITLE REVISION

1601.209 Whole Body Counting/Bioassay CHANGE

009-00

EN-RP-104 Personnel Contamination Events 3

EN-RP-108 Radiation Protection Posting 3

EN-RP-131 Air Sampling 1

EN-RP-203 Dose Assessment 0

EN-RP-208 Whole Body Counting and In-Vitro Bioassay 0

PL-182 Radiation Protection Expectations and Standards 1

Miscellaneous Document

Alpha Monitoring Plan, Revised August 22, 2006

A-7 Attachment

Section 4OA2: Identification and Resolution of Problems

CRs

ANO-2-2006-1535 ANO-2-2006-1655 ANO-2-2006-1891

ANO-2-2006-1625 ANO-2-2006-1693 ANO-2-2006-2174

Section 4OA3: Event Follow-up

Procedures

NUMBER TITLE REVISION

EN-DC-141 Design Inputs 2

EN-DC-313 Procurement Engineering Process 0

CRs

ANO-1-2006-1399 ANO-2-2006-1464 ANO-2-2006-2444 ANO-2-2006-2449

Section 4OA5: Other Activities (TI 2515/0166)

Safety Evaluation

FFN-06-008, Unit 2 RBS/ECCS Sump Strainer Replacement

A-8 Attachment

LIST OF ACRONYMS

ANO Arkansas Nuclear One

ASME American Society of Mechanical Engineers Boiler and Pressure Vessel Code

CAP corrective action program

CCW component cooling water

CFR Code of Federal Regulations

CR condition report

DSM digital speed monitor

EDG emergency diesel generator

EMI electromagnetic interference

FIN finding

MC manual chapter

MFP main feedwater pump

MSPI mitigating systems performance index

NCV noncited violation

NDE nondestructive examination

PI performance indicator

PWR pressurized water reactor

RCP reactor coolant pump

RCS reactor coolant system

RTP rated thermal power

SSCs system, structure, and components

TI temporary instruction

TS Technical Specification

UFSAR Updated Final Safety Analysis

URI unresolved item

A-9 Attachment