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{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION REGION III 2443 WARRENVILLE ROAD, SUITE 210 LISLE, IL 60532-4352  
{{#Wiki_filter:UNITED STATES
  October 29, 2010  
                            NUCLEAR REGULATORY COMMISSION
                                            REGION III
                              2443 WARRENVILLE ROAD, SUITE 210
Mr. Mark Bezilla Site Vice President  
                                        LISLE, IL 60532-4352
                                          October 29, 2010
Mr. Mark Bezilla
Site Vice President
FirstEnergy Nuclear Operating Company
Perry Nuclear Power Plant
P. O. Box 97, 10 Center Road, A-PY-A290
Perry, OH 44081-0097
SUBJECT:        PERRY NUCLEAR POWER PLANT NRC INTEGRATED
                INSPECTION REPORT 05000440/2010004
Dear Mr. Bezilla:
On September 30, 2010, the U.S. Nuclear Regulatory Commission (NRC) completed an
inspection at your Perry Nuclear Power Plant. The enclosed report documents the inspection
findings which were discussed on October 6, 2010, with you and members of your staff.
The inspection examined activities conducted under your license as they relate to safety and
compliance with the Commissions rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed
personnel.
Based on the results of this inspection, two NRC-identified findings of very low safety
significance (Green) were identified. Both of the findings were determined to involve a violation
of NRC requirements, however, because the findings were of very low safety significance and
because the issues were entered into your corrective action program, the NRC is treating the
findings as non-cited violations (NCVs) consistent with Section 2.3.2 of the NRC Enforcement
Policy.
If you contest the subject or severity of these NCVs, you should provide a response
within 30 days of the date of this inspection report, with the basis for your denial, to the
U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington,
DC 20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory
Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the
Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC
20555-0001; and the Resident Inspector Office at the Perry Nuclear Power Plant.
In addition, if you disagree with the cross-cutting aspect of any finding in this report, you
should provide a response within 30 days of the date of this inspection report, with the basis
for your disagreement, to the Regional Administrator, Region III, and the NRC Resident
Inspector at the Perry Nuclear Power Plant.


FirstEnergy Nuclear Operating Company
M. Bezilla                                    -2-
Perry Nuclear Power Plant
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its
P. O. Box 97, 10 Center Road, A-PY-A290
enclosure will be available electronically for public inspection in the NRC Public Document
Perry, OH  44081-0097
Room or from the Publicly Available Records (PARS) component of NRC's document system
SUBJECT: PERRY NUCLEAR POWER PLANT NRC INTEGRATED INSPECTION REPORT 05000440/2010004 Dear Mr. Bezilla:
(ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html
On September 30, 2010, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Perry Nuclear Power Plant. The enclosed report documents the inspection
(the Public Electronic Reading Room).
findings which were discussed on October 6, 2010, with you and members of your staff.  
                                              Sincerely,
                                              /RA/
                                              Jamnes L. Cameron, Chief
                                              Branch 6
                                              Division of Reactor Projects
Docket No. 50-440
License No. NPF-58
Enclosure:    Inspection Report 05000440/2010004
                w/Attachment: Supplemental Information
cc w/encl:    Distribution via ListServ


          U.S. NUCLEAR REGULATORY COMMISSION
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed
                          REGION III
personnel.  
Docket No:          50-440
License No:        NPF-58
Report No:          050000440/2010004
Licensee:          FirstEnergy Nuclear Operating Company (FENOC)
Facility:          Perry Nuclear Power Plant, Unit 1
Location:          Perry, Ohio
Dates:              July 1, 2010, through September 30, 2010
Inspectors:        M. Marshfield, Senior Resident Inspector
                    T. Hartman, Resident Inspector
                    R. Edwards, Reactor Inspector
                    L. Jones, Reactor Engineer
                    M. Phalen, Senior Health Physicist, DRS
                    W. Slawinski, Senior Health Physicist, DRS
                    P. Smagacz, Reactor Engineer
Observers:          V. Myers, Nuclear Safety Professional Development
                    Program
                    R. Leidy, Ohio Department of Health
Approved by:        Jamnes L. Cameron, Chief
                    Branch 6
                    Division of Reactor Projects
                                                                  Enclosure


   
                                          TABLE OF CONTENTS
Based on the results of this inspection, two NRC-identified findings of very low safety significance (Green) were identified. Both of the findings were determined to involve a violation of NRC requirements, however, because the findings were of very low safety significance and
SUMMARY OF FINDINGS ........................................................................................................... 1
because the issues were entered into your co
REPORT DETAILS ....................................................................................................................... 3
rrective action program, the NRC is treating the findings as non-cited violations (NCVs) consistent with Section 2.3.2 of the NRC Enforcement
  Summary of Plant Status ........................................................................................................... 3
Policy.  
  1.    REACTOR SAFETY ....................................................................................................... 3
If you contest the subject or severity of these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the
    1R01      Adverse Weather Protection (71111.01) ............................................................. 3
U.S. Nuclear Regulatory Commission, ATTN:  Document Control Desk, Washington,
    1R04      Equipment Alignment (71111.04Q) ..................................................................... 3
DC 20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory
    1R05      Fire Protection (71111.05Q)................................................................................ 5
Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector Office at the Perry Nuclear Power Plant.
    1R06      Flood Protection Measures (71111.06) ............................................................... 5
In addition, if you disagree with the cross-cutting aspect of any finding in this report, you
    1R11      Licensed Operator Requalification Program (71111.11) ..................................... 6
should provide a response within 30 days of the date of this inspection report, with the basis
    1R12      Maintenance Effectiveness (71111.12Q) ............................................................ 6
for your disagreement, to the Regional Administrator, Region III, and the NRC Resident Inspector at the Perry Nuclear Power Plant.     
    1R13      Maintenance Risk Assessments and Emergent Work Control (71111.13) ......... 7
  M. Bezilla    -2-
    1R15      Operability Evaluations (71111.15) ..................................................................... 8
    1R18      Temporary Plant Modifications (71111.18) ......................................................... 9
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its
    1R19      Post-Maintenance Testing (71111.19) ................................................................ 9
enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html
    1R22      Surveillance Testing (71111.22) ....................................................................... 10
  (the Public Electronic Reading Room).  
  2.    RADIATION SAFETY ................................................................................................... 13
Sincerely,   
    2RS1      Radiological Hazard Assessment and Exposure Controls (71124.01) ............. 13
      /RA/  Jamnes L. Cameron, Chief
    2RS3      In-Plant Airborne Radioactivity Control and Mitigation (71124.03) ................... 17
    2RS4      Occupational Dose Assessment (71124.04) ..................................................... 20
  4.    OTHER ACTIVITIES ..................................................................................................... 21
    4OA1      Performance Indicator Verification (71151)....................................................... 21
    4OA2      Problem Identification and Resolution (71152) ................................................. 23
    4OA3      Follow-up of Events and Notices of Enforcement Discretion (71153) ............... 26
    4OA5      Other Activities .................................................................................................. 27
    4OA6      Meetings............................................................................................................ 28
    4OA7      Licensee-Identified Violations ........................................................................... 28
SUPPLEMENTAL INFORMATION ............................................................................................... 1
  Key Points of Contact ................................................................................................................ 1
List of Items Opened, Closed and Discussed............................................................................ 1
  List of Documents Reviewed ..................................................................................................... 2
List of Acronyms Used .............................................................................................................. 8
                                                                                                                        Enclosure


Branch 6
                                        SUMMARY OF FINDINGS
Division of Reactor Projects
IR 05000440/2010004; 07/01/2010 - 09/30/2010; Surveillance Testing; Problem Identification
Docket No. 50-440
and Resolution.
License No. NPF-58
The inspection was conducted by resident and regional inspectors. The inspection report
(IR) covers a 3-month period of resident inspection. Two green findings which were NCVs were
identified. The significance of most findings is indicated by their color (Green, White, Yellow, or
Red) using Inspection Manual Chapter (IMC) 0609 Significance Determination Process (SDP).
Cross-cutting aspects were determined using IMC 0310, "Components Within The Cross-
Cutting Areas." Findings for which the SDP does not apply may be "Green," or be assigned a
severity level after NRC management review. The NRC's program for overseeing the safe
operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor
Oversight Process," Revision 4, dated December 2006.
A.      Inspector-Identified and Self-Revealed Findings
        Cornerstone: Mitigating Systems
    *    Green. The inspectors identified a finding of very low safety significance and associated
        NCV of 10 CFR 50, Appendix B, Criterion XI, Test Control, for the unacceptable
        preconditioning of the 'A' residual heat removal (RHR) pump minimum flow valve prior to
        quarterly in-service testing. Specifically, the licensee performed a surveillance that
        cycled the valve prior to performing stroke time testing, and had not previously
        performed an evaluation assessing the sequence for preconditioning. The licensee
        entered the issue into their corrective action program.
        The inspectors determined that unacceptably preconditioning the RHR minimum flow
        valve was a performance deficiency that affected the Mitigating Systems Cornerstone
        because it can mask the true as-found condition of a component designed to mitigate
        accidents. The performance deficiency was determined to be more than minor because,
        if left uncorrected, it could lead to a more significant safety concern. The finding was of
        very low safety significance because it was not a design/qualification deficiency, did not
        represent a loss of system safety function, did not result in a loss of function of a single
        train for greater than its Technical Specification (TS)-allowable outage time, did not
        result in a loss of function of nonsafety-related risk-significant equipment and was not
        risk significant due to external events. This finding has a cross-cutting aspect in the
        work control planning component of the Human Performance area (per
        IMC 0310 H.3(a)), because the licensee did not appropriately plan work activities for
        plant structures, systems, and components. Specifically, the licensee did not schedule
        the surveillance tests in the proper sequence to prevent unacceptable preconditioning of
        the valve. (Section 1R22)
    *    Green. The inspectors identified a finding of very low safety significance and associated
        NCV for a failure to comply with TS 3.0.2 by not entering TS Limiting Condition for
        Operation (LCO) 3.3.5.1 Condition A and TS LCO 3.3.6.1 Condition A when required.
        The inspectors determined that the licensee incorrectly utilized a TS Surveillance
        Requirement Note that allows a delay in entering the Conditions and Required Actions
        for the given TS LCO. As a result, the licensee failed to correctly enter the Conditions
        and Required Actions when reactor level instruments were declared inoperable to
                                                        1                                  Enclosure


  perform testing in support of planned maintenance. The licensee entered the issue
Enclosure: Inspection Report 05000440/2010004  w/Attachment:  Supplemental Information cc w/encl: Distribution via ListServ
  associated with the failure to comply with TS into their corrective action program.
 
  This performance deficiency was determined to be more than minor because it impacted
Enclosure U.S. NUCLEAR REGULATORY COMMISSION REGION III Docket No: 50-440 License No: NPF-58 Report No: 050000440/2010004
  the Equipment Performance attribute of the Mitigating Systems Cornerstone, and
Licensee: FirstEnergy Nuclear Operating Company (FENOC) 
  adversely affected the cornerstone objective to ensure the availability, reliability, and
Facility: Perry Nuclear Power Plant, Unit 1
  capability of systems that respond to initiating events to prevent undesirable
Location: Perry, Ohio
  consequences (i.e., core damage); and if left uncorrected it could lead to a more
Dates: July 1, 2010, through September 30, 2010 Inspectors: M. Marshfield, Senior Resident Inspector  T. Hartman, Resident Inspector
  significant safety concern. This finding is of very low safety significance because it was
R. Edwards, Reactor Inspector
  not a design/qualification deficiency, did not represent a loss of system safety function,
L. Jones, Reactor Engineer      M. Phalen, Senior Health Physicist, DRS      W. Slawinski, Senior Health Physicist, DRS      P. Smagacz, Reactor Engineer
  did not result in a loss of function of a single train for greater than its TS-allowable
  outage time, did not result in a loss of function of nonsafety-related risk-significant
  equipment and was not risk significant due to external events. This finding has a
  cross-cutting aspect in the decision making component of Human Performance
  cross-cutting area (per IMC 0310 H.1(a)), because the licensee did not use conservative
  assumptions to ensure the proposed action was safe. Specifically, the licensee
  incorrectly used the TS Surveillance Requirement Note to satisfy maintenance
  requirements. (Section 4OA2)
B. Licensee-Identified Violations
  One violation of very low safety significance was identified by the licensee and
  has been reviewed by the inspectors. Corrective actions taken or planned by the
  licensee have been entered into the licensee's corrective action program. This
  violation and its corrective action tracking number are listed in Section 4OA7 of
  this report.
                                                  2                                    Enclosure


                                        REPORT DETAILS
Summary of Plant Status
  Observers:  V. Myers, Nuclear Safety Professional Development        Program R. Leidy, Ohio Department of Health Approved by: Jamnes L. Cameron, Chief
The plant began the inspection period at 100 percent power. With the exception of minor
Branch 6
reductions in power to support routine surveillances and rod pattern adjustments, and several
Division of Reactor Projects 
occasions when the plant reduced power because of plant cooling limitations caused by
Enclosure TABLE OF CONTENTS SUMMARY OF FINDINGS ........................................................................................................... 1 REPORT DETAILS ................................................................................................................
summer environmental conditions, the plant remained at full power for the entire period.
....... 3Summary of Plant Status .......................................................................................................
1.     REACTOR SAFETY
.... 31.REACTOR SAFETY ....................................................................................................... 31R01Adverse Weather Protection (71111.01) ............................................................. 31R04Equipment Alignment (71111.04Q) ..................................................................... 31R05Fire Protection (71111.05Q)
      Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and
................................................................................ 51R06Flood Protection Measures (71111.06) ............................................................... 51R11Licensed Operator Requalification Program (71111.11) ..................................... 61R12Maintenance Effectiveness (71111.12Q) ............................................................ 61R13 Maintenance Risk Assessments and Emergent Work Control (71111.13) ......... 71R15Operability Evaluations (71111.15) ..................................................................... 81R18Temporary Plant Modifications (71111.18) ......................................................... 91R19Post-Maintenance Testing (71111.19) ................................................................ 91R22Surveillance Testing (71111.22) ....................................................................... 102.RADIATION SAFETY ................................................................................................... 132RS1Radiological Hazard Assessment and Exposure Controls (71124.01) ............. 132RS3In-Plant Airborne Radioactivity Control and Mitigation (71124.03) ................... 172RS4Occupational Dose Assessment (71124.04) ..................................................... 204.OTHER ACTIVITIES ..................................................................................................... 214OA1Performance Indicator Verification (71151)
      Emergency Preparedness
....................................................... 214OA2Problem Identification and Resolution (71152) ................................................. 234OA3Follow-up of Events and Notices of Enforcement Discretion (71153) ............... 264OA5Other Activities .................................................................................................. 274OA6Meetings............................................................................................................ 284OA7Licensee-Identified Violations ........................................................................... 28SUPPLEMENTAL INFORMATION ............................................................................................... 1Key Points of Contact .........................................................................................................
1R01 Adverse Weather Protection (71111.01)
....... 1List of Items Opened, Closed and Discussed
      External Flooding
............................................................................ 1List of Documents Reviewed ..................................................................................................... 2List of Acronyms Used .........................................................................................................
    a. Inspection Scope
..... 8 
      The inspectors evaluated the design, material condition, and procedures for coping with
  1 Enclosure SUMMARY OF FINDINGS IR 05000440/2010004; 07/01/2010 - 09/30/2010; Surveillance Testing; Problem Identification
      the design basis probable maximum flood. The evaluation included a review to check
and Resolution. The inspection was conducted by resident and regional inspectors. The inspection report (IR) covers a 3-month period of resident inspection. Two green findings which were NCVs were identified. The significance of most findings is indicated by their color (Green, White, Yellow, or Red) using Inspection Manual Chapter (IMC) 0609 "Significance Determination Process" (SDP)
      for deviations from the descriptions provided in the Updated Safety Analysis Report
Cross-cutting aspects were determined using IMC 0310, "Components Within The Cross-
      (USAR) for features intended to mitigate the potential for flooding from external factors.
Cutting Areas." Findings for which the SDP does not apply may be "Green," or be assigned a
      As part of this evaluation, the inspectors checked for obstructions that could prevent
severity level after NRC management review.  The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006. A. Inspector-Identified and Self-Revealed Findings
      draining, checked that the roofs did not contain obvious loose items that could clog
Cornerstone: Mitigating Systems
      drains in the event of heavy precipitation, and determined that barriers required to
  Green.  The inspectors identified a finding of very low safety significance and associated NCV of 10 CFR 50, Appendix B, Criterion XI, Test Control, for the unacceptable preconditioning of the 'A' residual heat removal (RHR) pump minimum flow valve prior to quarterly in-service testing.  Specifically, the licensee performed a surveillance that cycled the valve prior to performing stroke time testing, and had not previously
      mitigate the flood were in place and operable. Additionally, the inspectors performed a
performed an evaluation assessing the sequence for preconditioning.  The licensee
      walkdown of the protected area to identify any modification to the site which would inhibit
entered the issue into their corrective action program. 
      site drainage during a probable maximum precipitation event or allow water ingress past
      a barrier. The inspectors walked down underground bunkers/manholes subject to
      flooding that contained multiple train or multi-function risk-significant cables. The
      inspectors also reviewed the Off-Normal Instructions (ONIs) for mitigating the design
      basis flood to ensure it could be implemented as written.
      This inspection constituted one sample of external flooding as defined in Inspection
      Procedure (IP) 71111.01-05.
    b. Findings
      No findings were identified.
1R04 Equipment Alignment (71111.04Q)
  aInspection Scope
      The inspectors performed partial system walkdowns of the following risk-significant
      systems:
      *      'B' annulus exhaust gas treatment system (AEGTS) on July 7, 2010;
      *      'A' motor control center, switchgear and miscellaneous electrical equipment
              heating ventilation and air conditioning system on September 2, 2010; and
                                                    3                                    Enclosure


The inspectors determined that unacceptably preconditioning the RHR minimum flow valve was a performance deficiency that affected the Mitigating Systems Cornerstone  
    *        'B' reactor protection system (RPS) power supply electrical alignment while 'A'
because it can mask the true as-found condition of a component designed to mitigate
              RPS motor generator set was out of service on September 30, 2010.
accidents. The performance deficiency was determined to be more than minor because,  
    The inspectors selected these systems based on their risk-significance relative to the
if left uncorrected, it could lead to a more significant safety concern. The finding was of
    Reactor Safety Cornerstone at the time they were inspected. The inspectors attempted
very low safety significance because it was not a design/qualification deficiency, did not represent a loss of system safety function, did not result in a loss of function of a single train for greater than its Technical Specification (TS)-allowable outage time, did not
    to identify any discrepancies that could impact the function of the system, and, therefore,
result in a loss of function of nonsafety-related risk-significant equipment and was not
    potentially increase risk. The inspectors reviewed applicable operating procedures,
risk significant due to external events.  This finding has a cross-cutting aspect in the work control planning component of the Human Performance area (per IMC 0310 H.3(a)), because the licensee did not appropriately plan work activities for plant structures, systems, and components. Specifically, the licensee did not schedule the surveillance tests in the proper sequence to prevent unacceptable preconditioning of
    system diagrams, USAR, Technical Specification (TS) requirements, outstanding work
    orders (WOs), condition reports (CRs), and the impact of ongoing work activities on
    redundant trains of equipment in order to identify conditions that could have rendered
    the systems incapable of performing their intended functions. The inspectors also
    walked down accessible portions of the systems to verify system components and
    support equipment were aligned correctly and operable. The inspectors examined the
    material condition of the components and observed operating parameters of equipment
    to verify that there were no obvious deficiencies. The inspectors also verified that the
    licensee had properly identified and resolved equipment alignment problems that could
    cause initiating events or impact the capability of mitigating systems or barriers and
    entered them into the corrective action program (CAP) with the appropriate significance
    characterization. Documents reviewed are listed in the Attachment.
    These inspections constituted three partial system walkdown samples for equipment
    alignment as defined in IP 71111.04-05.
  b. Findings
    No findings were identified.
.2  Semi-Annual Complete System Walkdown
  a.  Inspection Scope
    On September 24, 2010, the inspectors concluded a complete system alignment
    inspection of the emergency closed cooling (ECC) system to verify the functional
    capability of the system. This system was selected because it was considered both
    safety significant and risk significant in the licensees probabilistic risk assessment.
    The inspectors walked down the system to review mechanical and electrical equipment
    line-ups, electrical power availability, system temperature indications, component
    labeling, component lubrication, component and equipment cooling, hangers and
    supports, operability of support systems, and to ensure that ancillary equipment or
    debris did not interfere with equipment operation. A review of a sample of past and
    outstanding WOs was performed to determine whether any deficiencies significantly
    affected the system function. In addition, the inspectors reviewed the CAP database to
    ensure that system equipment alignment problems were being identified and
    appropriately resolved. Documents reviewed are listed in the Attachment.
    This inspection constituted one complete system walkdown sample as defined in
    IP 71111.04-05.
b.  Findings
    No findings were identified.
                                                      4                                  Enclosure


the valve. (Section 1R22)  
1R05 Fire Protection (71111.05Q)
  a. Inspection Scope
      The inspectors conducted fire protection walkdowns which were focused on availability,
      accessibility, and the condition of firefighting equipment in the following risk-significant
      plant areas:
      *        Fire Zone 0IB-4; Intermediate Building 654'-6" Elevation;
      *        Fire Zone 0IB-3; Intermediate Bldg 620' Elevation;
      *        Fire Zone 0CC-2; Control Complex 599' Elevation;
      *        Fire Zone 0IB-1; Intermediate Bldg 574' Elevation; and
      *        Fire Zone 1AB-3B; Auxiliary Building 620'-6" Elevation West.
      The inspectors reviewed areas to assess if the licensee had implemented a fire
      protection program that adequately controlled combustibles and ignition sources within
      the plant, effectively maintained fire detection and suppression capability, maintained
      passive fire protection features in good material condition, and implemented adequate
      compensatory measures for out-of-service, degraded, or inoperable fire protection
      equipment, systems, or features in accordance with the licensees fire plan. The
      inspectors selected fire areas based on their overall contribution to internal fire risk as
      documented in the plants Individual Plant Examination of External Events with later
      additional insights, their potential to impact equipment which could initiate or mitigate a
      plant transient, or their impact on the plants ability to respond to a security event. Using
      the documents listed in the Attachment, the inspectors verified that fire hoses and
      extinguishers were in their designated locations and available for immediate use; that
      fire detectors and sprinklers were unobstructed; that transient material loading was
      within the analyzed limits; and fire doors, dampers, and penetration seals appeared to
      be in satisfactory condition. The inspectors also verified that minor issues identified
      during the inspection were entered into the licensees CAP. Documents reviewed are
      listed in the Attachment to this report.
      These activities constituted five quarterly fire protection inspection samples as defined in
      IP 71111.05-05.
  b. Findings
      No findings were identified.
1R06 Flood Protection Measures (71111.06)
  a.  Inspection Scope
      The inspectors reviewed selected risk important plant design features and licensee
      procedures intended to protect the plant and its safety-related equipment from internal
      flooding events. The inspectors reviewed flood analyses and design documents,
      including the USAR, engineering calculations, and ONI's to identify licensee
      commitments. The specific documents reviewed are listed in the Attachment to this
      report. In addition, the inspectors reviewed licensee drawings to identify areas and
      equipment that may be affected by internal flooding caused by the failure or
      misalignment of nearby sources of water, such as the fire suppression or the circulating
                                                      5                                  Enclosure


  Green. The inspectors identified a finding of very low safety significance and associated NCV for a failure to comply with TS 3.0.2 by not entering TS Limiting Condition for Operation (LCO) 3.3.5.1 Condition A and TS LCO 3.3.6.1 Condition A when requiredThe inspectors determined that the licensee incorrectly utilized a TS Surveillance
      water systems. The inspectors also reviewed the licensees corrective action documents
Requirement Note that allows a delay in entering the Conditions and Required Actions
      with respect to past flood-related items identified in the CAP to verify the adequacy of
for the given TS LCO.  As a result, the licensee failed to correctly enter the Conditions
      the corrective actions.
and Required Actions when reactor level instruments were declared inoperable to
      The inspectors performed a walkdown of the low pressure core spray areas to assess
  2 Enclosure perform testing in support of planned maintenance.  The licensee entered the issue associated with the failure to comply with TS into their corrective action program.  
      the adequacy of watertight doors and verify drains and sumps were clear of debris and
      were operable, and that the licensee complied with its commitments.
      This inspection constituted one internal flooding sample as defined in IP 71111.06-05.
  b. Findings
      No findings were identified.
1R11 Licensed Operator Requalification Program (71111.11)
  aInspection Scope
      On August 30, 2010, the inspectors observed a crew of licensed operators in the plants
      simulator during licensed operator requalification examinations to verify that operator
      performance was adequate, evaluators were identifying and documenting crew
      performance problems, and training was being conducted in accordance with licensee
      procedures. The inspectors evaluated the following areas:
      *        licensed operator performance;
      *        crews clarity and formality of communications;
      *        ability to take timely actions in the conservative direction;
      *        prioritization, interpretation, and verification of annunciator alarms;
      *        correct use and implementation of abnormal and emergency procedures;
      *        control board manipulations;
      *        oversight and direction from supervisors; and
      *        the ability to identify and implement appropriate TS actions and Emergency Plan
              actions and notifications.
      The crews performance in these areas was compared to pre-established operator action
      expectations and successful critical task completion requirements. Documents reviewed
      are listed in the Attachment to this report.
      This inspection constituted one quarterly operator license requalification program sample
      as defined in IP 71111.11.
  b. Findings
      No findings were identified.
1R12 Maintenance Effectiveness (71111.12Q)
  a. Inspection Scope
      The inspectors evaluated degraded performance issues involving the following
      risk-significant systems:
                                                        6                              Enclosure


This performance deficiency was determined to be more than minor because it impacted the Equipment Performance attribute of the Mitigating Systems Cornerstone, and
      *        'B' compressible gas mixing compressor;
adversely affected the cornerstone objective to ensure the availability, reliability, and
      *        'A' control room ventilation system;
capability of systems that respond to initiating events to prevent undesirable
      *        Division 3 emergency diesel generator (EDG) and high pressure core spray
consequences (i.e., core damage); and if left uncorrected it could lead to a more
              (HPCS) system; and
significant safety concern.  This finding is of very low safety significance because it was not a design/qualification deficiency, did not represent a loss of system safety function, did not result in a loss of function of a single train for greater than its TS-allowable
      *        Upper and lower containment airlocks.
outage time, did not result in a loss of function of nonsafety-related risk-significant
      The inspectors reviewed events such as where ineffective equipment maintenance had
equipment and was not risk significant due to external events.  This finding has a
      resulted in valid or invalid automatic actuations of engineered safeguards systems and
cross-cutting aspect in the decision making component of Human Performance cross-cutting area (per IMC 0310 H.1(a)), because the licensee did not use conservative assumptions to ensure the proposed action was safe.  Specifically, the licensee
      independently verified the licensee's actions to address system performance or condition
incorrectly used the TS Surveillance Requirement Note to satisfy maintenance
      problems in terms of the following:
requirements.  (Section 4OA2) B. Licensee-Identified Violations
      *        implementing appropriate work practices;
One violation of very low safety significance was identified by the licensee and has been reviewed by the inspectors.  Corrective actions taken or planned by the
      *        identifying and addressing common cause failures;
licensee have been entered into the licensee's corrective action program.  This
      *        scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;
violation and its corrective action tracking number are listed in Section 4OA7 of
      *        characterizing system reliability issues for performance;
this report.
      *        charging unavailability for performance;
 
      *        trending key parameters for condition monitoring;
  3 Enclosure REPORT DETAILS
      *        ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and
Summary of Plant Status
      *        verifying appropriate performance criteria for structures, systems, and
The plant began the inspection period at 100 percent power.  With the exception of minor reductions in power to support routine surveillances and rod pattern adjustments, and several
              components/functions classified as (a)(2), or appropriate and adequate goals and
occasions when the plant reduced power because of plant cooling limitations caused by summer environmental conditions, the plant remained at full power for the entire period. 1. REACTOR SAFETY
              corrective actions for systems classified as (a)(1).
Cornerstones:  Initiating Events, Mitigating Systems, Barrier Integrity, and Emergency Preparedness 1R01 Adverse Weather Protection (71111.01)
      The inspectors assessed performance issues with respect to the reliability, availability,
External Flooding
      and condition monitoring of the system. In addition, the inspectors verified maintenance
a. Inspection Scope
      effectiveness issues were entered into the CAP with the appropriate significance
The inspectors evaluated the design, material condition, and procedures for coping with the design basis probable maximum flood.  The evaluation included a review to check
      characterization. Documents reviewed are listed in the Attachment to this report.
for deviations from the descriptions provided in the Updated Safety Analysis Report (USAR) for features intended to mitigate the potential for flooding from external factors.  As part of this evaluation, the inspectors checked for obstructions that could prevent
      This inspection constituted four quarterly maintenance effectiveness samples as defined
draining, checked that the roofs did not contain obvious loose items that could clog
      in IP 71111.12-05.
drains in the event of heavy precipitation, and determined that barriers required to
  b. Findings
mitigate the flood were in place and operable.  Additionally, the inspectors performed a walkdown of the protected area to identify any modification to the site which would inhibit site drainage during a probable maximum precipitation event or allow water ingress past
      No findings were identified.
a barrier.  The inspectors walked down underground bunkers/manholes subject to
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)
flooding that contained multiple train or multi-function risk-significant cables.  The
  a. Inspection Scope
inspectors also reviewed the Off-Normal Instructions (ONIs) for mitigating the design basis flood to ensure it could be implemented as written.  This inspection constituted one sample of external flooding as defined in Inspection
      The inspectors reviewed the licensee's evaluation and management of plant risk for the
Procedure (IP) 71111.01-05. b. Findings
      maintenance and emergent work activities affecting risk-significant and safety-related
No findings were identified. 1R04 Equipment Alignment (71111.04Q) a. Inspection Scope
      equipment listed below to verify that the appropriate risk assessments were performed
The inspectors performed partial system walkdowns of the following risk-significant systems:  'B' annulus exhaust gas treatment
      prior to removing equipment for work:
system (AEGTS) on July 7, 2010;  'A' motor control center, switchgear and miscellaneous electrical equipment heating ventilation and air conditioning system on September 2, 2010; and 
      *        conservative grid operations on July 15, 2010;
  4 Enclosure  'B' reactor protection system (RPS) power supply electrical alignment while 'A' RPS motor generator set was out of service on September 30, 2010.    The inspectors selected these systems based on their risk-significance relative to the Reactor Safety Cornerstone at the time they were inspected.  The inspectors attempted
      *        work on control rod drive pump 'B' concurrent with testing of the Division 3 EDG
to identify any discrepancies that could impact the function of the system, and, therefore, potentially increase risk.  The inspectors reviewed applicable operating procedures, system diagrams, USAR, Technical Specification (TS) requirements, outstanding work
              on August 17, 2010;
orders (WOs), condition reports (CRs), and the impact of ongoing work activities on
      *        EDG fuel oil samples on August 26, 2010;
redundant trains of equipment in order to identify conditions that could have rendered
      *        reactor feed booster pump discharge check valve repair during the week of
the systems incapable of performing their intended functions.  The inspectors also
              September 13, 2010; and
walked down accessible portions of the systems to verify system components and support equipment were aligned correctly and operable.  The inspectors examined the material condition of the components and observed operating parameters of equipment
      *        HPCS diesel generator repairs during the week of September 15, 2010.
to verify that there were no obvious deficiencies.  The inspectors also verified that the
                                                    7                                    Enclosure
licensee had properly identified and resolved
equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the corrective action program (CAP) with the appropriate significance characterization.  Documents reviewed are listed in the Attachment. These inspections constituted three partial system walkdown samples for equipment alignment as defined in IP 71111.04-05. b. Findings
No findings were identified. .2 Semi-Annual Complete System Walkdown
a. Inspection Scope
On September 24, 2010, the inspectors concluded a complete system alignment inspection of the emergency closed cooling (ECC) system to verify the functional
capability of the system.  This system was selected because it was considered both safety significant and risk significant in
the licensee's probabilisti
c risk assessment.  The inspectors walked down the system to review mechanical and electrical equipment
line-ups, electrical power availability, system temperature indications, component labeling, component lubrication, component and equipment cooling, hangers and
supports, operability of support systems, and to ensure that ancillary equipment or debris did not interfere with equipment operation.  A review of a sample of past and outstanding WOs was performed to determine whether any deficiencies significantly affected the system function.  In addition, the inspectors reviewed the CAP database to
ensure that system equipment alignment problems were being identified and appropriately resolved.  Documents reviewed are listed in the Attachment. This inspection constituted one complete system walkdown sample as defined in
IP 71111.04-05. b. Findings
No findings were identified. 
  5 Enclosure 1R05 Fire Protection (71111.05Q) a. Inspection Scope
The inspectors conducted fire protection walkdowns which were focused on availability, accessibility, and the condition of firefighting equipment in the following risk-significant plant areas:  Fire Zone 0IB-4; Intermediate Building 654'-6" Elevation;  Fire Zone 0IB-3; Intermediate Bldg 620' Elevation;  Fire Zone 0CC-2; Control Complex 599' Elevation;  Fire Zone 0IB-1; Intermediate Bldg 574' Elevation; and  Fire Zone 1AB-3B; Auxiliary Building 620'-6" Elevation West. The inspectors reviewed areas to assess if the licensee had implemented a fire protection program that adequately controlled combustibles and ignition sources within
the plant, effectively maintained fire detection and suppression capability, maintained
passive fire protection features in good material condition, and implemented adequate
compensatory measures for out-of-service, degraded, or inoperable fire protection equipment, systems, or features in accordance with the licensee's fire plan.  The inspectors selected fire areas based on their overall contribution to internal fire risk as
documented in the plant's Individual Plant Examination of External Events with later
additional insights, their potential to impact equipment which could initiate or mitigate a
plant transient, or their impact on the plant's ability to respond to a security event.  Using the documents listed in the Attachment, the inspectors verified that fire hoses and extinguishers were in their designated locations and available for immediate use; that
fire detectors and sprinklers were unobstructed; that transient material loading was
within the analyzed limits; and fire doors, dampers, and penetration seals appeared to
be in satisfactory condition.  The inspectors also verified that minor issues identified during the inspection were entered into the licensee's CAP.  Documents reviewed are listed in the Attachment to this report. These activities constituted five quarterly fire protection inspection samples as defined in
IP 71111.05-05. b. Findings
No findings were identified. 1R06 Flood Protection Measures (71111.06) a. Inspection Scope
The inspectors reviewed selected risk important plant design features and licensee procedures intended to protect the plant and its safety-related equipment from internal
flooding events.  The inspectors reviewed flood analyses and design documents, including the USAR, engineering calculations, and ONI's to identify licensee commitments.  The specific documents reviewed are listed in the Attachment to this
report.  In addition, the inspectors reviewed licensee drawings to identify areas and
equipment that may be affected by internal flooding caused by the failure or
misalignment of nearby sources of water, such as the fire suppression or the circulating 
  6 Enclosure water systems.  The inspectors also reviewed the licensee's corrective action documents with respect to past flood-related items identified in the CAP to verify the adequacy of the corrective actions.  The inspectors performed a walkdown of the low pressure core spray areas to assess the adequacy of watertight doors and verify drains and sumps were clear of debris and
were operable, and that the licensee complied with its commitments. This inspection constituted one internal flooding sample as defined in IP 71111.06-05. b. Findings
No findings were identified. 1R11 Licensed Operator Requalification Program (71111.11) a. Inspection Scope
On August 30, 2010, the inspectors observed a crew of licensed operators in the plant's simulator during licensed operator requalification examinations to verify that operator
performance was adequate, evaluators were identifying and documenting crew
performance problems, and training was being conducted in accordance with licensee procedures.  The inspectors evaluated the following areas:  licensed operator performance;  crew's clarity and formality of communications;  ability to take timely actions in the conservative direction;  prioritization, interpretation, and verification of annunciator alarms;  correct use and implementation of abnormal and emergency procedures;  control board manipulations;  oversight and direction from supervisors; and  the ability to identify and implement appropriate TS actions and Emergency Plan actions and notifications. The crew's performance in these areas was compared to pre-established operator action expectations and successful critical task completion requirements.  Documents reviewed are listed in the Attachment to this report. This inspection constituted one quarterly operator license requalification program sample
as defined in IP 71111.11. b. Findings
No findings were identified. 1R12 Maintenance Effectiveness (71111.12Q) a. Inspection Scope
The inspectors evaluated degraded performance issues involving the following risk-significant systems: 
  7 Enclosure  'B' compressible gas mixing compressor;   'A' control room ventilation system;   Division 3 emergency diesel generator (EDG) and high pressure core spray (HPCS) system; and Upper and lower containment airlocks.  
The inspectors reviewed events such as where ineffective equipment maintenance had  
resulted in valid or invalid automatic actuations of engineered safeguards systems and  
independently verified the licensee's actions to address system performance or condition problems in terms of the following: implementing appropriate work practices; identifying and addressing common cause failures; scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule; characterizing system reliability issues for performance; charging unavailability for performance; trending key parameters for condition monitoring; ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and verifying appropriate performance criteria for structures, systems, and components/functions classified as (a)(2), or appropriate and adequate goals and corrective actions for systems classified as (a)(1). The inspectors assessed performance issues with respect to the reliability, availability, and condition monitoring of the system. In addition, the inspectors verified maintenance  
effectiveness issues were entered into the CAP with the appropriate significance characterization. Documents reviewed are listed in the Attachment to this report. This inspection constituted four quarterly maintenance effectiveness samples as defined in IP 71111.12-05. b. Findings
No findings were identified. 1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13) a. Inspection Scope
The inspectors reviewed the licensee's evaluation and management of plant risk for the maintenance and emergent work activities affecting risk-significant and safety-related  
equipment listed below to verify that the appropriate risk assessments were performed  


prior to removing equipment for work:  conservative grid operations on July 15, 2010;  work on control rod drive pump 'B' concurrent with testing of the Division 3 EDG on August 17, 2010;  EDG fuel oil samples on August 26, 2010;  reactor feed booster pump discharge check valve repair during the week of September 13, 2010; and  HPCS diesel generator repairs during the week of September 15, 2010. 
      These activities were selected based on their potential risk significance relative to the
  8 Enclosure These activities were selected based on their potential risk significance relative to the Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate and complete. When emergent work was performed, the inspectors verified that the plant risk was promptly reassessed and managed. The inspectors reviewed the scope  
      Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that
of maintenance work, discussed the results of the assessment with the licensee's  
      risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate
probabilistic risk analyst or shift technical advisor, and verified plant conditions were  
      and complete. When emergent work was performed, the inspectors verified that the
consistent with the risk assessment. The inspectors also reviewed TS requirements and  
      plant risk was promptly reassessed and managed. The inspectors reviewed the scope
walked down portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met. These maintenance risk assessments and emergent work control activities constituted  
      of maintenance work, discussed the results of the assessment with the licensee's
five samples as defined in IP 71111.13-05. b. Findings
      probabilistic risk analyst or shift technical advisor, and verified plant conditions were
No findings were identified. 1R15 Operability Evaluations (71111.15) a. Inspection Scope
      consistent with the risk assessment. The inspectors also reviewed TS requirements and
The inspectors reviewed the following issues: Technical Support Center ventilation with degraded flow turning vanes; EDG ventilation systems with installed relays beyond the 20-year qualification life; Emergency Closed Cooling cross-connect to fuel pool cooling and cleanup valve failed stroke time testing; and 'A' control room ventilation plenum missing insulation. The inspectors selected these potential operability issues based on the risk-significance of the associated components and systems. The inspectors evaluated the technical  
      walked down portions of redundant safety systems, when applicable, to verify risk
adequacy of the evaluations to ensure that TS operability was properly justified and the  
      analysis assumptions were valid and applicable requirements were met.
subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the TS and USAR to the licensee's evaluations to determine
      These maintenance risk assessments and emergent work control activities constituted
      five samples as defined in IP 71111.13-05.
  b. Findings
      No findings were identified.
1R15 Operability Evaluations (71111.15)
  a. Inspection Scope
      The inspectors reviewed the following issues:
      *        Technical Support Center ventilation with degraded flow turning vanes;
      *        EDG ventilation systems with installed relays beyond the 20-year qualification
              life;
      *        Emergency Closed Cooling cross-connect to fuel pool cooling and cleanup valve
              failed stroke time testing; and
      *        'A' control room ventilation plenum missing insulation.
      The inspectors selected these potential operability issues based on the risk-significance
      of the associated components and systems. The inspectors evaluated the technical
      adequacy of the evaluations to ensure that TS operability was properly justified and the
      subject component or system remained available such that no unrecognized increase in
      risk occurred. The inspectors compared the operability and design criteria in the
      appropriate sections of the TS and USAR to the licensees evaluations to determine
      whether the components or systems were operable. Where compensatory measures
      were required to maintain operability, the inspectors determined whether the measures
      in place would function as intended and were properly controlled. The inspectors
      determined, where appropriate, compliance with bounding limitations associated with the
      evaluations. Additionally, the inspectors reviewed a sampling of corrective action
      documents to verify that the licensee was identifying and correcting any deficiencies
      associated with operability evaluations. Documents reviewed are listed in the
      Attachment to this report.
      This operability inspection constituted four samples as defined in IP 71111.15-05.
  b.  Findings
      No findings were identified.
                                                      8                                    Enclosure


whether the components or systems were
1R18 Temporary Plant Modifications (71111.18)
operable.  Where compensatory measures were required to maintain operability, the inspectors determined whether the measures
  a. Inspection Scope
in place would function as intended and were properly controlled.  The inspectors
      The inspectors reviewed the temporary modification for the Hot Surge Tank Hi/Low
determined, where appropriate, compliance with bounding limitations associated with the evaluations.  Additionally, the inspectors reviewed a sampling of corrective action documents to verify that the licensee was identifying and correcting any deficiencies
      Level Alarm. The inspectors compared the temporary configuration changes and
associated with operability evaluations.  Documents reviewed are listed in the Attachment to this report. This operability inspection constituted four samples as defined in IP 71111.15-05. b. Findings
      associated 10 CFR 50.59 screening and evaluation information against the design basis,
No findings were identified. 
      the USAR, and the TS, as applicable, to verify that the modification did not affect the
  9 Enclosure 1R18 Temporary Plant Modifications (71111.18) a. Inspection Scope
      operability or availability of the affected system(s). The inspectors also compared the
The inspectors reviewed the temporary modification for the Hot Surge Tank Hi/Low Level Alarm. The inspectors compared the temporary configuration changes and associated 10 CFR 50.59 screening and evaluation information against the design basis,  
      licensees information to operating experience information to ensure that lessons learned
the USAR, and the TS, as applicable, to verify that the modification did not affect the  
      from other utilities had been incorporated into the licensees decision to implement the
operability or availability of the affected system(s). The inspectors also compared the  
      temporary modification. The inspectors, as applicable, performed field verifications to
licensee's information to operating experience information to ensure that lessons learned  
      ensure that the modifications were installed as directed; the modifications operated as
from other utilities had been incorporated into the licensee's decision to implement the temporary modification. The inspectors, as applicable, performed field verifications to ensure that the modifications were installed as directed; the modifications operated as  
      expected; modification testing adequately demonstrated continued system operability,
expected; modification testing adequately demonstrated continued system operability,  
      availability, and reliability; and that operation of the modifications did not impact the
availability, and reliability; and that operation of the modifications did not impact the  
      operability of any interfacing systems. Lastly, the inspectors discussed the temporary
operability of any interfacing systems. Lastly, the inspectors discussed the temporary modification with operations, engineering, and training personnel to ensure that the individuals were aware of how extended operation with the temporary modification in  
      modification with operations, engineering, and training personnel to ensure that the
place could impact overall plant performance. Documents reviewed in the course of this inspection are listed in the Attachment to this report. This inspection constituted one sample of a temporary modification as defined in  
      individuals were aware of how extended operation with the temporary modification in
IP 71111.18-05. b. Findings
      place could impact overall plant performance. Documents reviewed in the course of this
No findings were identified. 1R19 Post-Maintenance Testing (71111.19) a. Inspection Scope
      inspection are listed in the Attachment to this report.
The inspectors reviewed the following post-maintenance (PM) activities to verify that procedures and test activities were adequate to ensure system operability and functional capability: safety relief valve control switch replacement during the week of August 2, 2010; high drywell pressure master trip unit replacement during the week of August 9, 2010; AEGTS fan replacement during the week of August 25, 2010; emergency service water (ESW) ventilation system outlet damper hydramotor work during the week of September 7, 2010; HPCS pump breaker relay replacement during the week of September 17, 2010;  
      This inspection constituted one sample of a temporary modification as defined in
and Division 3 EDG outage retest during the week of September 24, 2010. These activities were selected based upon the structure, system, or component's ability to impact risk. The inspectors evaluated these activities for the following (as applicable): the effect of testing on the plant had been adequately addressed;   testing was adequate for the maintenance performed;  
      IP 71111.18-05.
  10 Enclosure acceptance criteria were clear and demonstrated operational readiness;  test instrumentation was appropriate;  tests were performed as written in accordance with properly reviewed and approved procedures;  equipment was returned to its operational status following testing (temporary modifications or jumpers required for test performance were properly removed after test completion); and  test documentation was properly evaluated.  The inspectors evaluated the activities against TS, the USAR, 10 CFR Part 50
  b. Findings
requirements, licensee procedures, and various NRC generic communications to ensure that the test results adequately ensured that the equipment met the licensing basis and
      No findings were identified.
design requirements.  In addition, the inspectors reviewed corrective action documents
1R19 Post-Maintenance Testing (71111.19)
associated with PM tests to determine whether the licensee was identifying problems and entering them in the CAP and that the problems were being corrected
  a. Inspection Scope
commensurate with their importance to safety.  Documents reviewed are listed in the Attachment to this report. This inspection constituted six PM testing samples as defined in IP 71111.19-05. b. Findings
      The inspectors reviewed the following post-maintenance (PM) activities to verify that
No findings were identified. 1R22 Surveillance Testing (71111.22) a. Inspection Scope
      procedures and test activities were adequate to ensure system operability and functional
The inspectors reviewed the test results for the following activities to determine whether risk-significant systems and equipment were capable of performing their intended safety function and to verify testing was conducted in accordance with applicable procedural
      capability:
      *      safety relief valve control switch replacement during the week of August 2, 2010;
      *      high drywell pressure master trip unit replacement during the week of
              August 9, 2010;
      *      AEGTS fan replacement during the week of August 25, 2010;
      *      emergency service water (ESW) ventilation system outlet damper hydramotor
              work during the week of September 7, 2010;
      *      HPCS pump breaker relay replacement during the week of September 17, 2010;
              and
      *      Division 3 EDG outage retest during the week of September 24, 2010.
      These activities were selected based upon the structure, system, or component's ability
      to impact risk. The inspectors evaluated these activities for the following (as applicable):
      *      the effect of testing on the plant had been adequately addressed;
      *      testing was adequate for the maintenance performed;
                                                      9                                  Enclosure


and TS requirements: Residual Heat Removal (RHR) 'A' pump and valve inservice testing during the week of July 12, 2010 (IST); Emergency Service Water (ESW) 'C' pump and valve operability test during the week of July 23, 2010 (routine);   Reactor Core Isolation Cooling (RCIC) pump and valve operability test during the week of August 2, 2010 (routine); and   ESW 'B' pump and valve operability testing during the week of August 13, 2010 (routine). The inspectors observed in-plant activities and reviewed procedures and associated records to determine the following:   did preconditioning occur;   were the effects of the testing adequately addressed by control room personnel or engineers prior to the commencement of the testing; were acceptance criteria clearly stated, demonstrated operational readiness, and consistent with the system design basis; plant equipment calibration was correct, accurate, and properly documented;
      *      acceptance criteria were clear and demonstrated operational readiness;
  11 Enclosure as-left setpoints were within required ranges, and the calibration frequency were in accordance with TS, the USAR, procedures, and applicable commitments;  measuring and test equipment calibration was current;  test equipment was used within the required range and accuracy;  applicable prerequisites described in the test procedures were satisfied;  test frequencies met TS requirements to demonstrate operability and reliability;  tests were performed in accordance with the test procedures and other applicable procedures;  jumpers and lifted leads were controlled and restored where used;  test data and results were accurate, complete, within limits, and valid;  test equipment was removed after testing;  where applicable for IST activities, testing was performed in accordance with the applicable version of Section XI, American Society of Mechanical Engineers (ASME) Code, and reference values were consistent with the system design
      *      test instrumentation was appropriate;
basis;  where applicable, test results not meeting acceptance criteria were addressed
      *      tests were performed as written in accordance with properly reviewed and
with an adequate operability evaluation or the system or component was declared inoperable;  where applicable for safety-related instrument control surveillance tests, reference setting data were accurately incorporated in the test procedure;  where applicable, actual conditions encountering high resistance electrical contacts were such that the intended safety function could still be accomplished;  prior procedure changes had not provided an opportunity to identify problems encountered during the performance of the surveillance or calibration test;  equipment was returned to a position or status required to support the performance of its safety functions; and  all problems identified during the testing were appropriately documented and dispositioned in the CAP.  Documents reviewed are listed in the Attachment to this report. This inspection constituted three routine surveillance testing samples and one inservice testing sample as defined in IP 71111.22, Sections -02 and -05. b. Findings
              approved procedures;
Introduction:  The inspectors identified a finding of very low safety significance (Green) and associated NCV of 10 CFR Part 50, Appendix B, Criterion XI, Test Control, for
      *      equipment was returned to its operational status following testing (temporary
unacceptable preconditioning of the 'A' RHR pump minimum flow valve prior to quarterly
              modifications or jumpers required for test performance were properly removed
IST.  Specifically, the surveillance test sequencing caused this valve to be opened and closed before the documented stroke time testing, and the sequence had not been evaluated for preconditioning prior to performance of the tests.
              after test completion); and
      *      test documentation was properly evaluated.
Description:  On July 8, 2010, at approximately 9:30 a.m., the inspectors observed the performance of surveillance test SVI-E12-T2001, RHR A Pump and Valve Operability
      The inspectors evaluated the activities against TS, the USAR, 10 CFR Part 50
      requirements, licensee procedures, and various NRC generic communications to ensure
      that the test results adequately ensured that the equipment met the licensing basis and
      design requirements. In addition, the inspectors reviewed corrective action documents
      associated with PM tests to determine whether the licensee was identifying problems
      and entering them in the CAP and that the problems were being corrected
      commensurate with their importance to safety. Documents reviewed are listed in the
      Attachment to this report.
      This inspection constituted six PM testing samples as defined in IP 71111.19-05.
  b. Findings
      No findings were identified.
1R22 Surveillance Testing (71111.22)
  a. Inspection Scope
      The inspectors reviewed the test results for the following activities to determine whether
      risk-significant systems and equipment were capable of performing their intended safety
      function and to verify testing was conducted in accordance with applicable procedural
      and TS requirements:
      *      Residual Heat Removal (RHR) 'A' pump and valve inservice testing during the
              week of July 12, 2010 (IST);
      *      Emergency Service Water (ESW) 'C' pump and valve operability test during the
              week of July 23, 2010 (routine);
      *      Reactor Core Isolation Cooling (RCIC) pump and valve operability test during the
              week of August 2, 2010 (routine); and
      *      ESW 'B' pump and valve operability testing during the week of August 13, 2010
              (routine).
      The inspectors observed in-plant activities and reviewed procedures and associated
      records to determine the following:
      *      did preconditioning occur;
      *      were the effects of the testing adequately addressed by control room personnel
              or engineers prior to the commencement of the testing;
      *      were acceptance criteria clearly stated, demonstrated operational readiness, and
              consistent with the system design basis;
      *      plant equipment calibration was correct, accurate, and properly documented;
                                                  10                                  Enclosure


Test.  Included in this test is the quarterly timed valve stroke of 1E12-F0064A, RHR Pump A Min Flow Valve, as required by the IST program.  During review of the previous shift narrative logs, it was identified that surveillance test SVI-E12-T1194, LPCI (Low Pressure Core Injection) Pump A Discharge Low Flow (Bypass) Channel Functional for
  *      as-left setpoints were within required ranges, and the calibration frequency were
1E12-N652A, was performed at around 1:30 a.m.  This surveillance calibrates 
          in accordance with TS, the USAR, procedures, and applicable commitments;
  12 Enclosure instrument 1E12-N652A, LPCI Pump A Discharge Low Flow Instrument.  The calibration of the low flow instrument results in the 'A' train RHR pump minimum flow valve stroking. 
  *      measuring and test equipment calibration was current;
This sequence of testing fully cycled the valve several times less than 8 hours prior to obtaining the IST stroke timing data during SVI-E12-T2001.
  *      test equipment was used within the required range and accuracy;
Inspection Manual Technical Guidance 9900 defines unacceptable preconditioning, in  
  *      applicable prerequisites described in the test procedures were satisfied;
part, as "The alteration; variation; manipulation; or adjustment of the physical condition
  *      test frequencies met TS requirements to demonstrate operability and reliability;
of a structure, system, and component (SSC) before or during TS surveillance or ASME Code testing that will alter one or more of an SSC's operational parameters, which results in acceptable test results.  Such changes could mask the actual as-found condition of the SSC and possibly result in an inability to verify the operability of the
  *        tests were performed in accordance with the test procedures and other
SSC.  In addition, unacceptable preconditioning could make it difficult to determine
          applicable procedures;
whether the SSC would perform its intended function during an event in which the SSC
  *      jumpers and lifted leads were controlled and restored where used;
might be needed."  Technical Guidance 9900 further describes that some types of preconditioning may be considered acceptable, but that "this preconditioning should have been evaluated and documented in advance of the surveillance."  Since the
  *      test data and results were accurate, complete, within limits, and valid;
licensee had not performed an evaluation which justified that preconditioning of the valve
  *      test equipment was removed after testing;
was acceptable prior to completing the testing, the licensee's surveillance testing
  *      where applicable for IST activities, testing was performed in accordance with the
sequence that cycled the valve prior to obtaining stroke time data constituted unacceptable preconditioning of the valve.
          applicable version of Section XI, American Society of Mechanical Engineers
Additionally, the unacceptable preconditioning of the RHR valve was not in accordance with the licensee's procedural guidance regarding IST.  Licensee Nuclear Operating
          (ASME) Code, and reference values were consistent with the system design
Procedure (NOP)-ER-3204, "Inservice Testing Program," states, in part, "Maintenance
          basis;
activities should not be scheduled to influence the results of upcoming tests.  Such actions, known as preconditioning, should be avoided."  In addition it also states, in part, "Care should be taken to ensure that procedures, surveillances, or tasks are not scheduled such that unacceptable preconditioning of a component prior to the inservice
  *      where applicable, test results not meeting acceptance criteria were addressed
test occurs.  Where unacceptable preconditioning would occur, the procedure/task
          with an adequate operability evaluation or the system or component was
should specify that an as found test be performed first."
          declared inoperable;
The licensee performed an investigation which revealed that, historically, these two
  *      where applicable for safety-related instrument control surveillance tests,
surveillances had been completed in either sequence without significant differences in
          reference setting data were accurately incorporated in the test procedure;
measured stroke time.  As a result, the licensee determined that the preconditioning did
  *      where applicable, actual conditions encountering high resistance electrical
not significantly affect the IST stroke timing of the valve.  The licensee used this
          contacts were such that the intended safety function could still be accomplished;
information to support an operability declaration for the system.
  *      prior procedure changes had not provided an opportunity to identify problems
Analysis:  The inspectors determined that stroking of the RHR minimum flow valve prior to as-found stroke timing constituted unacceptable preconditioning and a performance
          encountered during the performance of the surveillance or calibration test;
deficiency. Specifically, performing the IST surveillance test in this sequence may not accurately indicate potential valve degradation.  The inspectors determined that the performance deficiency affected the Mitigating Systems Cornerstone, because it could mask the true as-found condition of a component designed to mitigate accidents. The
  *      equipment was returned to a position or status required to support the
inspectors evaluated the performance deficiency in accordance with Inspection Manual
          performance of its safety functions; and
Change (IMC) 0612, Appendix B, "Issue Screening."  This performance deficiency was
  *      all problems identified during the testing were appropriately documented and
compared to, and was not similar to any o
          dispositioned in the CAP.
f, the examples in IMC 0612, Appendix E, "Examples of Minor Issues," but was characterized as more than minor because, if left uncorrected, it could lead to a more significant safety concern.
  Documents reviewed are listed in the Attachment to this report.
The inspectors determined the finding could be evaluated using the SDP in  
  This inspection constituted three routine surveillance testing samples and one inservice
accordance with IMC 0609, "Significance Determination Process," Attachment 0609.04,
  testing sample as defined in IP 71111.22, Sections -02 and -05.
  13 Enclosure "Phase 1 - Initial Screening and Characterization of Findings," Table 3b for the Mitigating Systems Cornerstone.  The inspectors determined the finding was of very low risk
b. Findings
significance because it was not a design/qualification deficiency, did not represent a loss of system safety function, did not result in a loss of function of a single train for greater than its TS allowable outage time, did not result in a loss of function of nonsafety-related
  Introduction: The inspectors identified a finding of very low safety significance (Green)
risk-significant equipment, and was not risk significant due to external events.
  and associated NCV of 10 CFR Part 50, Appendix B, Criterion XI, Test Control, for
This finding has a cross-cutting aspect in the work control planning component of the
  unacceptable preconditioning of the 'A' RHR pump minimum flow valve prior to quarterly
Human Performance cross-cutting area (per IMC 0310 H.3(a)), because the licensee did not appropriately plan work activities for plant SSCs and components.  Specifically, the licensee did not schedule the surveillance tests in the proper sequence to prevent
  IST. Specifically, the surveillance test sequencing caused this valve to be opened and
unacceptable preconditioning of the valve.
  closed before the documented stroke time testing, and the sequence had not been
Enforcement:  Title 10 CFR Part 50, Appendix B, Criterion XI, Test Control, states, in part, that "A test program shall be established to assure that all testing required to demonstrate that structures, systems, and components will perform satisfactorily in service is identified and performed in accordance with written test procedures which
  evaluated for preconditioning prior to performance of the tests.
incorporate the requirements and acceptance limits contained in applicable design
  Description: On July 8, 2010, at approximately 9:30 a.m., the inspectors observed the
documents."  Contrary to this requirement, on July 8, 2010, the licensee stroked 1E12-F0064A, RHR Pump A Min Flow Valve for test procedure SVI-E12-T1194 prior to performing IST stroke timing, and failed to prevent unacceptable pre-conditioning of the  
  performance of surveillance test SVI-E12-T2001, RHR A Pump and Valve Operability
pump minimum flow valve. Because this finding is of very low safety significance and  
  Test. Included in this test is the quarterly timed valve stroke of 1E12-F0064A, RHR
because it was entered into the licensee's CAP as CR 10-79624, this violation is being
  Pump A Min Flow Valve, as required by the IST program. During review of the previous
treated as an Non-Cited Violation (NCV) consistent with Section 2.3.2 of the NRC
  shift narrative logs, it was identified that surveillance test SVI-E12-T1194, LPCI (Low
Enforcement Policy.  (NCV 05000440/2010004-01; Unacceptable Preconditioning of
  Pressure Core Injection) Pump A Discharge Low Flow (Bypass) Channel Functional for
RHR Valve Prior to ASME In-Service Testing.) 2. RADIATION SAFETY Cornerstones:  Public and Occupational Radiation Safety 2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01) The inspection activities supplement those documented in Inspection Report (IR) 05000440/2010003, and constitute one complete sample as defined in
  1E12-N652A, was performed at around 1:30 a.m. This surveillance calibrates
IP 71124.01-05.  .1 Radiological Hazard Assessment (02.02) a. Inspection Scope
                                                  11                                Enclosure
The inspectors determined if there had been changes to plant operations since the last inspection that could result in a significant new radiological hazard for onsite workers or
members of the public.  The inspectors evaluated whether the licensee assessed the
potential impact of these changes and has implemented periodic monitoring, as appropriate, to detect and quantify the radiological hazard. The inspectors reviewed the last two radiological surveys from selected plant areas.  The inspectors evaluated whether the thoroughness and frequency of the surveys were appropriate for the given radiological hazards.
  14 Enclosure The inspectors conducted walkdowns of the facility, including radioactive waste processing, storage, and handling areas to evaluate material conditions and performed independent radiation measurements to verify conditions. The inspectors observed work in potential airborne areas and evaluated whether the air samples were representative of the breathing air zone.  The inspectors evaluated whether continuous air monitors were located in areas with low background to minimize false alarms and representative of actual work areas.  The inspectors evaluated the
licensee's program for monitoring levels of loose surface contamination in areas of the plant with the potential for the contamination to become airborne. b. Findings
No findings were identified. .2 Instructions to Workers (02.03) a. Inspection Scope
The inspectors selected various containers holding nonexempt licensed radioactive materials that may cause unplanned or inadvertent exposure of workers, and assessed
whether the containers were labeled and controlled in accordance with 10 CFR 20.1904,  
"Labeling Containers," or met the requirements of 10 CFR 20.1905(g). For work activities that could suddenly and severely increase radiological conditions, the inspectors assessed the licensee's means to inform workers of changes that could significantly impact their occupational dose. b. Findings
No findings were identified. .3 Contamination and Radioactive Material Control (02.04) a. Inspection Scope
The inspectors observed several locations where the licensee monitors potentially contaminated material leaving the radiologically controlled area and evaluated the
methods used for the control, survey, and release of materials from these areas.  The
inspectors also observed the performance of personnel surveying and releasing material for unrestricted use to determine if the methods used were in accordance with procedures and whether those procedures were sufficient to control the spread of
contamination and prevent unintended release of materials from the site. The inspectors
determined whether radiation monitoring instrumentation used for these surveys had appropriate sensitivity for the types of radiation present. The inspectors reviewed the licensee's criteria for the survey and release of potentially contaminated material to determine if there was guidance on how to respond to an alarm that indicates the presence of licensed radioactive material. The inspectors reviewed the licensee's procedures and records to verify that the radiation detection instrumentation was used at its typical sensitivity level based on 
  15 Enclosure appropriate counting parameters.  The inspectors assessed whether or not the licensee established a de facto "release limit" by altering the instrument's typical sensitivity through such methods as raising the energy discriminator level or locating the instrument
in a high-radiation background area. The inspectors selected three sealed sources from the licensee's inventory records and assessed whether the sources were accounted for and verified to be intact (i.e., they were not leaking their radioactive content). The inspectors evaluated whether any transactions, since the last inspection, involving nationally tracked sources were reported in accordance with 10 CFR 20.2207. b. Findings
No findings were identified. .4 Radiological Hazards Control and Work Coverage (02.05) a. Inspection Scope
The inspectors evaluated ambient radiological conditions (e.g., radiation levels or potential radiation levels) during tours of the facility.  The inspectors assessed whether
the conditions were consistent with applicable posted surveys, radiation work permits
(RWPs), and worker briefings.  The inspectors reviewed RWPs for work within airborne
radioactivity areas with the potential for individual worker internal exposures.  For these RWPs, the inspectors evaluated airborne radioactive controls and monitoring, including potential for significant airborne levels (e.g., grinding, grit blasting, system breaches, entry into tanks, cubicles, and reactor cavities).  The inspectors assessed barrier (e.g.,
tent or glove box) integrity and temporary high-efficiency particulate air (HEPA) ventilation system operation for selected airborne radioactive material areas The inspectors examined the licensee's physical and programmatic controls for highly activated or contaminated materials (nonfuel) stored within spent fuel and other storage pools.  The inspectors assessed whether appropriate controls (i.e., administrative and physical controls) were in place to preclude inadvertent removal of these materials from the pool.  The inspectors examined the posting and physical controls for selected high-radiation areas (HRAs) and very-high-radiation areas (VHRAs) to verify conformance with the occupational performance indicator (PI). b. Findings
  No findings were identified. .5 Risk-Significant High-Radiation Area and Very High-Radiation Area Controls (02.06) a. Inspection Scope
The inspectors discussed with the radiation protection (RP) manager the controls and procedures for HRAs and VHRAs. The inspectors discussed methods employed by the
licensee to provide stricter control of VHRA access as specified in 10 CFR 20.1602, 
  16 Enclosure "Control of Access to Very High-Radiation Areas," and Regulatory Guide 8.38, "Control of Access to High and Very High-Radiation Areas of Nuclear Plants."  The inspectors
assessed whether any changes to licensee procedures substantially reduced the effectiveness and level of worker protection.  The inspectors discussed the controls in place for special areas that have the potential to become VHRAs during certain plant operations with first-line health physics (HP) supervisors (or equivalent positions having backshift HP oversight authority).  The
inspectors assessed whether these plant operations required communication
beforehand with the HP group, so as to allow corresponding timely actions to properly post, control, and monitor the radiation hazards including re-access authorization. The inspectors evaluated licensee controls for VHRAs and areas with the potential to become a VHRA to ensure that an individual was not able to gain unauthorized access


to the VHRA. b. Findings
instrument 1E12-N652A, LPCI Pump A Discharge Low Flow Instrument. The calibration
No findings were identified. .6 Radiation Worker Performance (02.07) a. Inspection Scope
of the low flow instrument results in the 'A' train RHR pump minimum flow valve stroking.
The inspectors observed radiation worker performance with respect to stated RP work requirements. The inspectors assessed whether workers were aware of the radiological conditions in their workplace and the RWP controls/limits in place, and whether their performance reflected the level of radiological hazards present. The inspectors reviewed a maximum of 10 radiological problem reports since the last inspection that found the cause of the event to be human performance errors. The
This sequence of testing fully cycled the valve several times less than 8 hours prior to
inspectors evaluated whether there was an observable pattern traceable to a similar cause. The inspectors assessed whether this perspective matched the corrective action approach taken by the licensee to resolve
obtaining the IST stroke timing data during SVI-E12-T2001.
the reported problems. The inspectors discussed with the RP manager any problems with the corrective actions planned or taken. b. Findings
Inspection Manual Technical Guidance 9900 defines unacceptable preconditioning, in
No findings were identified. .7 Radiation Protection Technician Proficiency (02.08) a. Inspection Scope
part, as The alteration; variation; manipulation; or adjustment of the physical condition
The inspectors observed the performance of the RP technicians with respect to all RP work requirements. The inspectors evaluated whether technicians were aware of the  
of a structure, system, and component (SSC) before or during TS surveillance or ASME
radiological conditions in their workplace and the RWP controls/limits, and whether their
Code testing that will alter one or more of an SSCs operational parameters, which
performance was consistent with their training and qualifications with respect to the  
results in acceptable test results. Such changes could mask the actual as-found
radiological hazards and work activities.
condition of the SSC and possibly result in an inability to verify the operability of the
  17 Enclosure The inspectors reviewed a maximum of 10 radiological problem reports since the last inspection that found the cause of the event to be RP technician error. The inspectors
SSC. In addition, unacceptable preconditioning could make it difficult to determine
whether the SSC would perform its intended function during an event in which the SSC
might be needed. Technical Guidance 9900 further describes that some types of
preconditioning may be considered acceptable, but that this preconditioning should
have been evaluated and documented in advance of the surveillance. Since the
licensee had not performed an evaluation which justified that preconditioning of the valve
was acceptable prior to completing the testing, the licensees surveillance testing
sequence that cycled the valve prior to obtaining stroke time data constituted
unacceptable preconditioning of the valve.
Additionally, the unacceptable preconditioning of the RHR valve was not in accordance
with the licensees procedural guidance regarding IST. Licensee Nuclear Operating
Procedure (NOP)-ER-3204, Inservice Testing Program, states, in part, Maintenance
activities should not be scheduled to influence the results of upcoming tests. Such
actions, known as preconditioning, should be avoided. In addition it also states, in part,
Care should be taken to ensure that procedures, surveillances, or tasks are not
scheduled such that unacceptable preconditioning of a component prior to the inservice
test occurs. Where unacceptable preconditioning would occur, the procedure/task
should specify that an as found test be performed first.
The licensee performed an investigation which revealed that, historically, these two
surveillances had been completed in either sequence without significant differences in
measured stroke time. As a result, the licensee determined that the preconditioning did
not significantly affect the IST stroke timing of the valve. The licensee used this
information to support an operability declaration for the system.
Analysis: The inspectors determined that stroking of the RHR minimum flow valve prior
to as-found stroke timing constituted unacceptable preconditioning and a performance
deficiency. Specifically, performing the IST surveillance test in this sequence may not
accurately indicate potential valve degradation. The inspectors determined that the
performance deficiency affected the Mitigating Systems Cornerstone, because it could
mask the true as-found condition of a component designed to mitigate accidents. The
inspectors evaluated the performance deficiency in accordance with Inspection Manual
Change (IMC) 0612, Appendix B, Issue Screening. This performance deficiency was
compared to, and was not similar to any of, the examples in IMC 0612, Appendix E,
Examples of Minor Issues, but was characterized as more than minor because, if left
uncorrected, it could lead to a more significant safety concern.
The inspectors determined the finding could be evaluated using the SDP in
accordance with IMC 0609, Significance Determination Process, Attachment 0609.04,
                                              12                                  Enclosure


evaluated whether there was an observable pattern traceable to a similar cause.  The inspectors assessed whether this perspective matched the corrective action approach taken by the licensee to resolve the reported problems. b. Findings
      Phase 1 - Initial Screening and Characterization of Findings, Table 3b for the Mitigating
No findings were identified. 2RS3 In-Plant Airborne Radioactivity Control and Mitigation (71124.03) The inspection activities supplement those documented in IR 05000440/2010003, and constitute one complete sample as defined in IP 71124.03-05.  .1 Inspection Planning (02.01) a. Inspection Scope
      Systems Cornerstone. The inspectors determined the finding was of very low risk
The inspectors reviewed the plant USAR to identify areas of the plant designed as potential airborne radiation areas and any
      significance because it was not a design/qualification deficiency, did not represent a loss
associated ventilation systems or airborne monitoring instrumentation.  Instrumentation review included continuous air monitors
      of system safety function, did not result in a loss of function of a single train for greater
(continuous air monitors and particulate-iodine-noble-gas-type instruments) used to
      than its TS allowable outage time, did not result in a loss of function of nonsafety-related
identify changing airborne radiological conditions such that actions to prevent an
      risk-significant equipment, and was not risk significant due to external events.
overexposure may be taken.  The review included an overview of the respiratory
      This finding has a cross-cutting aspect in the work control planning component of the
protection program and a description of the types of devices used.  The inspectors reviewed USAR, TS, and emergency planning documents to identify location and quantity of respiratory protection devices stored for emergency use. The inspectors reviewed the licensee's procedures for maintenance, inspection, and use of respiratory protection equipment including self-contained breathing apparatus
      Human Performance cross-cutting area (per IMC 0310 H.3(a)), because the licensee did
(SCBA). Additionally, the inspectors reviewed procedures for air quality maintenance and the reported PIs to identify any related to unintended dose resulting from intakes of radioactive materials. b. Findings
      not appropriately plan work activities for plant SSCs and components. Specifically, the
No findings were identified. .2 Engineering Controls (02.02) a. Inspection Scope
      licensee did not schedule the surveillance tests in the proper sequence to prevent
The inspectors reviewed the licensee's use of permanent and temporary ventilation to determine whether the licensee used ventilation systems as part of its engineering controls (in lieu of respiratory protection devices) to control airborne radioactivity.  The inspectors reviewed procedural guidance for use of installed plant systems, such as
      unacceptable preconditioning of the valve.
containment purge, spent fuel pool ventilation, and auxiliary building ventilation, and
      Enforcement: Title 10 CFR Part 50, Appendix B, Criterion XI, Test Control, states, in
assessed whether the systems are used, to the extent practicable, during high-risk activities (e.g., using containment purge during cavity flood up). 
      part, that A test program shall be established to assure that all testing required to
  18 Enclosure The inspectors selected installed ventilation systems used to mitigate the potential for  
      demonstrate that structures, systems, and components will perform satisfactorily in
airborne radioactivity, and evaluated whether the ventilation airflow capacity, flow path (including the alignment of the suction and discharges), and filter/charcoal unit efficiencies, as appropriate, were consistent with maintaining concentrations of airborne radioactivity in work areas below the concentrations of an airborne area to the extent practicable. The inspectors selected temporary ventilation system setups (HEPA/charcoal negative pressure units, down draft tables, tents, metal "Kelly buildings," and other enclosures)
      service is identified and performed in accordance with written test procedures which
used to support work in contaminated areas.  The inspectors assessed whether the use
      incorporate the requirements and acceptance limits contained in applicable design
of these systems was consistent with licensee procedural guidance and as-low-as-is-
      documents. Contrary to this requirement, on July 8, 2010, the licensee stroked
reasonably-achievable (ALARA) concepts. b. Findings
      1E12-F0064A, RHR Pump A Min Flow Valve for test procedure SVI-E12-T1194 prior to
No findings were identified. .3 Use of Respiratory Protection Devices (02.03) a. Inspection Scope
      performing IST stroke timing, and failed to prevent unacceptable pre-conditioning of the
For those situations where it is impractical to employ engineering controls to minimize airborne radioactivity, the inspectors assessed whether the licensee provided respiratory protective devices such that occupational doses are ALARA.  The inspectors selected
      pump minimum flow valve. Because this finding is of very low safety significance and
work activities where respiratory protection devices were used to limit the intake of
      because it was entered into the licensees CAP as CR 10-79624, this violation is being
radioactive materials, and assessed whether the licensee performed an evaluation
      treated as an Non-Cited Violation (NCV) consistent with Section 2.3.2 of the NRC
concluding that further engineering controls were not practical and that the use of respirators was ALARA.  The inspectors also evaluated whether the licensee had established means (such as routine bioassay) to determine if the level of protection
      Enforcement Policy. (NCV 05000440/2010004-01; Unacceptable Preconditioning of
(protection factor) provided by the respiratory protection devices during use was at least as good as that assumed in the licensee's work controls and dose assessment. The inspectors assessed whether respiratory protection devices used to limit the intake of radioactive materials were certified by the National Institute for Occupational Safety
      RHR Valve Prior to ASME In-Service Testing.)
and Health/Mine Safety and Health Administration (NIOSH/MSHA) or have been approved by the NRC in accordance with 10 CFR 20.1703(b).  The inspectors selected work activities where respiratory protection devices were used.  The inspectors
2.     RADIATION SAFETY
evaluated whether the devices were used consistent with their NIOSH/MSHA certification or any conditions of their NRC approval. The inspectors reviewed records of air testing for supplied-air devices and SCBA bottles to assess whether the air used in these devices meets or exceeds Grade D quality. The
      Cornerstones: Public and Occupational Radiation Safety
inspectors reviewed plant breathing air supply systems to determine whether they meet the minimum pressure and airflow requirements for the devices in use. The inspectors selected individuals qualified to use respiratory protection devices, and assessed whether they have been deemed fit to use the devices by a physician.  The inspectors selected several individuals assigned to wear a respiratory protection
2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01)
device and observed them donning, doffing, and functionally checking the device as appropriate.  Through interviews with these individuals, the inspectors evaluated
      The inspection activities supplement those documented in Inspection Report
whether they knew how to safely use t
      (IR) 05000440/2010003, and constitute one complete sample as defined in
he device and how to properly respond to any 
      IP 71124.01-05.
  19 Enclosure device malfunction or unusual occurrence (loss of power, loss of air, etc.)The inspectors reviewed training curricula for users of the devices. The inspectors chose various respiratory protection devices staged and ready for use in the plant or stocked for issuance.  The inspectors assessed the physical condition of the
  .1  Radiological Hazard Assessment (02.02)
device components (mask or hood, harnesses, air lines, regulators, air bottles, etc.) and reviewed records of routine inspection for each.  The inspectors selected several of the devices and reviewed records of maintenance on the vital components (e.g., pressure
    a. Inspection Scope
regulators, inhalation/exhalation valves, hose couplings). The inspectors assessed
      The inspectors determined if there had been changes to plant operations since the last
whether onsite personnel assigned to repair vital components had received vendor-
      inspection that could result in a significant new radiological hazard for onsite workers or
provided training. b. Findings
      members of the public. The inspectors evaluated whether the licensee assessed the
No findings were identified. .4 Self-Contained Breathing Apparatus for Emergency Use (02.04) a. Inspection Scope
      potential impact of these changes and has implemented periodic monitoring, as
Based on USAR, TS, and emergency operating procedure requirements, the inspectors reviewed the status and surveillance records of SCBAs staged in-plant for use during emergencies.  The inspectors reviewed the licensee's capability for refilling and transporting SCBA air bottles to and from the control room and operations support center during emergency conditions. The inspectors selected individuals on control room shift crews, and individuals from designated departments currently assigned emergency duties (e.g., onsite search and
      appropriate, to detect and quantify the radiological hazard.
rescue duties) to assess whether control room operators and other emergency response
      The inspectors reviewed the last two radiological surveys from selected plant areas.
and RP personnel (assigned in-plant search and rescue duties or as required by emergency operating procedures or the emergency plan) were trained and qualified in the use of SCBAs (including personal bottle change out). The inspectors evaluated whether personnel assigned to refill bottles were trained and qualified for that task. The inspectors determined whether appropriate mask sizes and types were available for use (i.e., in-field mask size and type matched what was used in fit-testing).  The
      The inspectors evaluated whether the thoroughness and frequency of the surveys were
inspectors selected various on-shift operators to determine whether they have no facial hair that would interfere with the sealing of the mask to the face and whether vision
      appropriate for the given radiological hazards.
correction (e.g., glasses inserts or corrected lenses) were available as appropriate. The inspectors reviewed the past 2 years of maintenance records for several SCBA units used to support operator activities during accident conditions and designated as "ready for service" to assess whether any maintenance or repairs on any SCBA unit's vital components were performed by an individual, or individuals, certified by the  
                                                      13                                    Enclosure
manufacturer of the device to perform the work. The vital components typically are the
pressure-demand air regulator and the low-pressure alarm.  The inspectors reviewed the  
onsite maintenance procedures governing vital component work to determine any inconsistencies with the SCBA manufacturer's recommended practices.  For those SCBAs designated as "ready for service," the inspectors determined whether the  
required, periodic air cylinder hydrostatic testing was documented and up to date, and
the retest air cylinder markings required by the U.S. Department of Transportation were in place. 
  20 Enclosure b. Findings
No findings were identified. .5 Problem identification and Resolution (02.05) a. Inspection Scope
The inspectors reviewed CRs and other corrective action documents to determine whether problems associated with control and mitigation of in-plant airborne radioactivity
were being identified at the appropriate threshold and were properly addressed for  
resolution in the licensee's CAP. b. Findings
No findings were identified 2RS4 Occupational Dose Assessment (71124.04) This inspection constituted a partial sample as defined in IP 71124.04-05.  .1 Inspection Planning (02.01) a. Inspection Scope
The inspectors reviewed the results of RP program audits related to internal and external dosimetry (e.g., licensee's quality assurance audits, self-assessments, or other
independent audits) to gain insights into overall licensee performance in the area of dose
assessment and focus the inspection activities consistent with the principle of "smart


sampling." b. Findings
    The inspectors conducted walkdowns of the facility, including radioactive waste
No findings were identified. .2 Internal Dosimetry (02.03) Internal Dose Assessment - Airborne Monitoring
    processing, storage, and handling areas to evaluate material conditions and performed
a. Inspection Scope
    independent radiation measurements to verify conditions.
The inspectors reviewed the licensee's program
    The inspectors observed work in potential airborne areas and evaluated whether the air
for airborne radioactivity assessment and dose assessment, as applicable, based on airborne monitoring and calculations of  
    samples were representative of the breathing air zone. The inspectors evaluated
derived air concentration. The inspectors determined whether flow rates and collection
    whether continuous air monitors were located in areas with low background to minimize
times for air sampling equipment were adequate to allow lower limits of detection to be obtained. The inspectors also reviewed the adequacy of procedural guidance to assess internal dose if respiratory protection was used.  The licensee had not performed dose
    false alarms and representative of actual work areas. The inspectors evaluated the
assessments using airborne/derived air concentration monitoring since the last inspection.
    licensees program for monitoring levels of loose surface contamination in areas of the
   21 Enclosure b. Findings
    plant with the potential for the contamination to become airborne.
No findings were identified. .3 Special Dosimetric Situations (02.04) Dosimeter Placement and Assessment of Effective Dose Equivalent for External
   b. Findings
Exposures. a. Inspection Scope
    No findings were identified.
The inspectors reviewed the licensee's methodology for monitoring external dose in non-uniform radiation fields or where large dose gradients exist. The inspectors evaluated the licensee's criteria for determining when alternate monitoring, such as use of multi-badging, was to be implemented. The inspectors reviewed dose assessments performed using multi-badging to evaluate whether the assessment was performed consistent with licensee procedures and dosimetric standards. b. Findings
.2  Instructions to Workers (02.03)
No findings were identified. 4. OTHER ACTIVITIES 4OA1 Performance Indicator Verification (71151) .1 Mitigating Systems Performance Index - Heat Removal System
  a. Inspection Scope
a. Inspection Scope
    The inspectors selected various containers holding nonexempt licensed radioactive
The inspectors sampled licensee submittals for the Mitigating Systems Performance Index (MSPI) - Heat Removal System performance indicator
    materials that may cause unplanned or inadvertent exposure of workers, and assessed
for the period from the third quarter 2009 through the second quarter 2010.  To determine the accuracy of the PI
    whether the containers were labeled and controlled in accordance with 10 CFR 20.1904,
data reported during those periods, PI definitions and guidance contained in the Nuclear Energy Institute (NEI) Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 6, dated October 2009, were used.  The inspectors reviewed the  
    Labeling Containers, or met the requirements of 10 CFR 20.1905(g).
licensee's operator narrative logs, issue reports, event reports, MSPI derivation reports, and NRC Integrated Inspection Reports for the period of the third quarter 2009 through
    For work activities that could suddenly and severely increase radiological conditions, the
the second quarter 2010 to validate the accuracy of the submittals. The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, that the change was in  
    inspectors assessed the licensees means to inform workers of changes that could
accordance with applicable NEI guidance.  The inspectors also reviewed the licensee's
    significantly impact their occupational dose.
issue report database to determine if any problems had been identified with the PI data
  b. Findings
collected or transmitted for this indicator and none were identified.  Documents reviewed are listed in the Attachment to this report. This inspection constituted one MSPI heat removal system sample as defined in
    No findings were identified.
IP 71151-05. 
.3  Contamination and Radioactive Material Control (02.04)
  22 Enclosure b. Findings
  a. Inspection Scope
No findings of significance were identified. .2 Mitigating Systems Performance Index - Residual Heat Removal System
    The inspectors observed several locations where the licensee monitors potentially
a. Inspection Scope
    contaminated material leaving the radiologically controlled area and evaluated the
The inspectors sampled licensee submittals for the MSPI - Residual Heat Removal System performance indicator for the period from the third quarter 2009 through the second quarter 2010.  To determine the accuracy of the PI data reported during those
    methods used for the control, survey, and release of materials from these areas. The
periods, PI definitions and guidance contained in the Nuclear Energy Institute (NEI)
    inspectors also observed the performance of personnel surveying and releasing material
    for unrestricted use to determine if the methods used were in accordance with
    procedures and whether those procedures were sufficient to control the spread of
    contamination and prevent unintended release of materials from the site. The inspectors
    determined whether radiation monitoring instrumentation used for these surveys had
    appropriate sensitivity for the types of radiation present.
    The inspectors reviewed the licensees criteria for the survey and release of potentially
    contaminated material to determine if there was guidance on how to respond to an alarm
    that indicates the presence of licensed radioactive material.
    The inspectors reviewed the licensees procedures and records to verify that the
    radiation detection instrumentation was used at its typical sensitivity level based on
                                                  14                                  Enclosure


Document 99-02, "Regulatory Assessment Performance Indicator Guideline,"
    appropriate counting parameters. The inspectors assessed whether or not the licensee
Revision 6, dated October 2009, were used. The inspectors reviewed the licensee's
    established a de facto release limit by altering the instruments typical sensitivity
operator narrative logs, issue reports, MSPI
    through such methods as raising the energy discriminator level or locating the instrument
derivation reports, event reports and NRC Integrated Inspection Reports for the period of the third quarter 2009 through the second
    in a high-radiation background area.
quarter 2010 to validate the accuracy of the submittals. The inspectors reviewed the  
    The inspectors selected three sealed sources from the licensees inventory records and
MSPI component risk coefficient to determine if it had changed by more than 25 percent
    assessed whether the sources were accounted for and verified to be intact (i.e., they
in value since the previous inspection, and if so, that the change was in accordance with
    were not leaking their radioactive content).
applicable NEI guidance. The inspectors also reviewed the licensee's issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified. Documents reviewed are listed in the Attachment to this report. This inspection constituted one MSPI residual heat removal system sample as defined in
    The inspectors evaluated whether any transactions, since the last inspection, involving
IP 71151-05. b. Findings
    nationally tracked sources were reported in accordance with 10 CFR 20.2207.
No findings of significance were identified. .2 Mitigating Systems Performanc
  b. Findings
e Index - Cooling Water Systems
    No findings were identified.
a. Inspection Scope
.4  Radiological Hazards Control and Work Coverage (02.05)
The inspectors sampled licensee submittals for the MSPI - Cooling Water Systems performance indicator for the period from the third quarter 2009 through the second quarter 2010. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in the NEI Document 99-02, "Regulatory
  a. Inspection Scope
Assessment Performance Indicator Guideline," Revision 6, dated October 2009, were
    The inspectors evaluated ambient radiological conditions (e.g., radiation levels or
used. The inspectors reviewed the licensee's operator narrative logs, issue reports,  
    potential radiation levels) during tours of the facility. The inspectors assessed whether
MSPI derivation reports, event reports and
    the conditions were consistent with applicable posted surveys, radiation work permits
NRC Integrated Inspection Reports for the period of the third quarter 2009 through the second quarter 2010 to validate the accuracy of the submittals. The inspectors reviewed the MSPI component risk
    (RWPs), and worker briefings. The inspectors reviewed RWPs for work within airborne
coefficient to determine if it had changed by more than 25 percent in value since the  
    radioactivity areas with the potential for individual worker internal exposures. For these
previous inspection, and if so, that the change was in accordance with applicable NEI
    RWPs, the inspectors evaluated airborne radioactive controls and monitoring, including
guidance. The inspectors also reviewed the licensee's issue report database to
    potential for significant airborne levels (e.g., grinding, grit blasting, system breaches,
determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified. Documents reviewed are listed in the Attachment to this report. 
    entry into tanks, cubicles, and reactor cavities). The inspectors assessed barrier (e.g.,
  23 Enclosure This inspection constituted one MSPI cooling water system sample as defined in
    tent or glove box) integrity and temporary high-efficiency particulate air (HEPA)
IP 71151-05. b. Findings
    ventilation system operation for selected airborne radioactive material areas
No findings of significance were identified. 4OA2 Problem Identification and Resolution (71152) Cornerstones:  Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and
    The inspectors examined the licensees physical and programmatic controls for highly
Physical Protection .1 Routine Review of Items Entered Into the CAP
    activated or contaminated materials (nonfuel) stored within spent fuel and other storage
a. Inspection Scope
    pools. The inspectors assessed whether appropriate controls (i.e., administrative and
As part of the various baseline inspection procedures discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities
    physical controls) were in place to preclude inadvertent removal of these materials from
and plant status reviews to verify that they were being entered into the licensee's CAP at
    the pool.
an appropriate threshold, that adequate attention was being given to timely corrective
    The inspectors examined the posting and physical controls for selected high-radiation
actions, and that adverse trends were identified and addressed. Attributes reviewed
    areas (HRAs) and very-high-radiation areas (VHRAs) to verify conformance with the
included:  identification of the problem was complete and accurate; timeliness was
    occupational performance indicator (PI).
commensurate with the safety significance; evaluation and disposition of performance issues, generic implications, common causes, contributing factors, root causes, extent-of-condition reviews, and previous occurrences reviews were proper and
  b. Findings
adequate; and that the classification, prioritization, focus, and timeliness of corrective
    No findings were identified.
actions were commensurate with safety and sufficient to prevent recurrence of the issue. Minor issues entered into the licensee's CAP as a result of the inspectors' observations are included in the Attachment to this report.   These routine reviews for the identification and resolution of problems did not constitute any additional inspection samples. Instead, by procedure they were considered an
.5  Risk-Significant High-Radiation Area and Very High-Radiation Area Controls (02.06)
integral part of the inspections performed during the quarter and documented in Section 1 of this report. b. Findings
   a. Inspection Scope
No findings were identified. .2 Daily Corrective Action Program Reviews
    The inspectors discussed with the radiation protection (RP) manager the controls and
a. Inspection Scope
    procedures for HRAs and VHRAs. The inspectors discussed methods employed by the
In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of
    licensee to provide stricter control of VHRA access as specified in 10 CFR 20.1602,
items entered into the licensee's CAP.  This review was accomplished through
                                                    15                                    Enclosure
inspection of the station's daily CR packages. These daily reviews were performed by procedure as part of the inspectors' daily plant status monitoring activities and, as such, did not constitute any separate inspection samples. 
  24 Enclosure b. Findings
No findings were identified. .3 Semi-Annual Trend Review
a. Inspection Scope
The inspectors performed a review of the licensee's CAP and associated documents to identify trends that could indicate the existence of a more significant safety issue. The
inspectors' review was focused on repetitive equipment issues, but also considered the results of daily inspector CAP item screening discussed in Section 4OA2.2 above, licensee trending efforts, and licensee human performance results.  The inspectors'
review nominally considered the 6-month period from January 2010 through June 2010,
although some examples expanded beyond those dates where the scope of the trend
warranted. The reviews also included issues documented outside of the normal CAP in major equipment problem lists, repetitive and/or rework maintenance lists, departmental problem/challenges lists, system health reports, quality assurance audit/surveillance reports, self-assessment reports, and maintenance rule assessments.  The inspectors
compared and contrasted their results with the results contained in the licensee's
CAP trending reports.  Corrective actions associated with a sample of the issues identified in the licensee's trending reports were reviewed for adequacy. This review constituted a single semi-annual trend inspection sample as defined in
IP 71152-05. b. Findings
No findings were identified. .4 In-depth Review- Technical Specifications Compliance
a. Inspection Scope
The inspectors performed an annual follow-up of selected issues sample of the licensee's process for performing and documenting TS compliance.  The inspectors reviewed documentation in the licensee's CAP, official narrative operating logs and LCO tracking module, for compliance with site-specific administrative, operational, and
licensing procedures specifically to assess for proper control and documentation of the
entry and exit of LCO Conditions and Required Actions.  Documents reviewed are listed
in the Attachment to this report.
This review constituted one in-depth problem identification and resolution sample as defined in IP 71152-05. b. Findings
Introduction:  The inspectors identified a finding of very low safety significance (Green) and an associated NCV for the licensee's failure to follow the requirements of TS
LCO 3.0.2 by not entering TS LCO 3.3.5.1 Condition A and TS 3.3.6.1 Condition A when 
   25 Enclosure reactor vessel level instruments 1B21N0673C and 1B21N0674C were declared inoperable.  Technical Specification LCO 3.0.2 requires that "Upon discovery of a failure
to meet an LCO, the Required Actions of the associated Conditions shall be met, except as provided in LCO 3.0.5 and LCO 3.0.6."
Description:  On August 9, 2010, during a review of operator narrative logs, the inspectors noted a log entry that identified the use of a TS Surveillance Requirement
(SR) Note to support the performance of WO #200322765, "PDP - 'New PM' Replace
Rosemount STU Card."  This WO included a step to acquire as-found data of the card being replaced prior to its removal.  The method of acquiring this as-found data included performing portions of surveillance test procedure SVI-B21-T0187C, ECCS/HPCS RPV
Water Level 2 and Level 8 Channel C Functional for 1B21-N673C.  Additionally, this WO step stated, "Sign Off/Close Surveillance Instruction as No Credit."  Surveillance test
SVI-B21-T0187C renders Reactor Vessel Level instruments 1B21N0673C and 1B21N0674C inoperable.  This surveillance references the TS Surveillance Notes associated with SR 3.3.5.1 and 3.3.6.1.  These SR Notes state, in part, "When a channel
is placed in an inoperable status solely for performance of required Surveillances, entry
into associated Conditions and Required Actions may be delayed."  The licensee utilized
the SR Note during the performance of as-found checks using the surveillance and did not enter the Conditions and Required Actions for the 22 minutes it took to perform the test. 
The inspectors reviewed the licensee's use of the surveillance notes and determined
that the delay in entering the Conditions and Required Actions was inappropriate
because the surveillance was being performed to satisfy WO requirements, not
TS-required SRs.  As a result, the licensee declared the instruments inoperable but did not enter the Conditions or Required Actions for the associated LCOs.  This is contrary to the requirements of TS LCO 3.0.2 which states "Upon discovery of a failure
to meet an LCO, the Required Actions of the associated Conditions shall be met, except
as provided in LCO 3.0.5 and LCO 3.0.6."  Limiting Condition of Operation 3.0.5 and
LCO 3.0.6 did not apply in this situation.
An additional review of recent narrative log entries identified several instances of
misapplication of the same surveillance notes. The longest time period the LCO was not
adhered to was 4 hours and 47 minutes.  In combination with the replacement and
subsequent operability testing, the instrument(s) were inoperable on several different
occasions, for a sum total of 13 hours and 29 minutes. The LCO allows the instrument(s) to be inoperable for up to 24 hours before any additional actions are required.  The inspectors did not identify any instances where the LCO Required Action times were


exceeded.
    Control of Access to Very High-Radiation Areas, and Regulatory Guide 8.38, Control
Analysis:  The inspectors determined that the licensee's failure to follow TS LCO 3.0.2 constituted a performance deficiency.  Specifically, the licensee did not enter the LCOs and Required Actions for inoperable TS equipment.  The inspectors evaluated the
    of Access to High and Very High-Radiation Areas of Nuclear Plants. The inspectors
performance deficiency in accordance with IMC 0612, Appendix B, "Issue Screening.
    assessed whether any changes to licensee procedures substantially reduced the
This performance deficiency was not similar to any of the examples in IMC 0612, Appendix E, "Examples of Minor Issues," but was characterized as more than minor
    effectiveness and level of worker protection.
because it impacted the Equipment Performance attribute of the Mitigating Systems Cornerstone, and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent
    The inspectors discussed the controls in place for special areas that have the potential
undesirable consequences (i.e., core damage); and if left uncorrected it could lead to a
    to become VHRAs during certain plant operations with first-line health physics (HP)
more significant safety concern. 
    supervisors (or equivalent positions having backshift HP oversight authority). The
  26 Enclosure
    inspectors assessed whether these plant operations required communication
The inspectors determined the finding could be evaluated using the SDP in accordance
    beforehand with the HP group, so as to allow corresponding timely actions to properly
with IMC 0609, "Significance Determination Process," Attachment 0609.04, "Phase 1 - Initial Screening and Characterization of findings," Table 3b for the Mitigating Systems Cornerstone. The inspectors determined the finding was of very low safety significance
    post, control, and monitor the radiation hazards including re-access authorization.
(Green) because it was not a design/qualification deficiency, did not represent a loss of
    The inspectors evaluated licensee controls for VHRAs and areas with the potential to
system safety function, did not result in a loss of function of a single train for greater than
    become a VHRA to ensure that an individual was not able to gain unauthorized access
its TS-allowable outage time, did not result in a loss of function of nonsafety-related
    to the VHRA.
risk-significant equipment and was not risk significant due to external events.
  b. Findings
This finding has a cross-cutting aspect in the decision making component of the Human
    No findings were identified.
Performance cross-cutting area (per IMC 0310 H.1(b)), because the licensee did not use conservative assumptions to ensure the proposed action was safe. Specifically, the
.6  Radiation Worker Performance (02.07)
licensee incorrectly used the TS SR Note to satisfy maintenance requirements.
Enforcement:  The inspectors determined that the finding represents a violation of regulatory requirements because it involved improper implementation of TS.  The
licensee utilized TS SR Notes while performing surveillances to satisfy maintenance
WOs.  In accordance with TS LCO 3.0.2, in these cases entry into TS LCO 3.3.5.1 Condition A and 3.3.6.1 Condition A is required.  Contrary to the above, the licensee did not enter the Conditions and Required Actions immediately upon declaring TS-required instrumentation inoperable.  Because this finding is of very low safety significance and 
because it was entered into the licensee's CAP as CR 10-81162, this violation is being
treated as an NCV consistent with Section 2.3.2 of the NRC Enforcement Policy. 
(NCV 05000440/2010004-02; Failure to Comply with Technical Specification LCOs When Reactor Vessel Level Instruments Were Declared Inoperable.)
4OA3 Follow-up of Events and Notices of Enforcement Discretion (71153) .1 (Closed) Licensee Event Report 05000440/2010-003:  Loss of Control Rod Drive Header Pressure Results in Manual RPS Actuation
a. Inspection Scope
On May 11, 2010, a manual actuation of RPS was inserted to comply with TS because of multiple accumulators being inoperable coincident with the inability to restore control  
rod drive (CRD) charging header pressure.  A trip unit failure caused an invalid
loss-of-coolant accident (LOCA) initiation signal and resulted in the load shed of the
XH12 stub bus.  Due to an abnormal electrical lineup, both CRD pumps tripped and they were unable to be restarted.  The licensee replaced the trip unit and restored the CRD system to its normal configuration. The licensee documented the failed equipment in
CR 10-76727.  The inspectors reviewed this Licensee Event Report (LER) and did not
identify any findings or violations of NRC requirements.  Documents reviewed as part of this inspection are listed in the attachment.  This LER is closed. This event follow-up review constituted one sample as defined in IP 71153-05. 
  27 Enclosure .2 (Closed) Retraction of Event Notification 45815:  Loss of Safety Function to Control the Release of Radioactive Material
a. Inspection Scope
On April 6, 2010, the licensee initiated an event notification (EN) related to a loss of safety function involving five containment isolation valves.  Specifically, the licensee reported that they had a potential loss of safety function for the ability to control the
release of radioactive material.  This was due to a loss of power to the LOCA isolation
logic associated with containment penetration single valve isolations. On June 6, 2010, the licensee retracted this notification.  The licensee evaluated the condition and determined the containment penetrations were still able to perform their design function.  The inspectors reviewed the information contained in the evaluation, and did not identify
any findings or violations related to the licensee's retraction. This EN retraction is closed. This event follow-up review constituted one sample as defined in IP 71153-05. 4OA5 Other Activities
.1 (Closed) Unresolved Item 05000440/2010003-06:  Failure to Perform a Hydrostatic Test
in Accordance with ASME Code
   a. Inspection Scope
   a. Inspection Scope
  This Unresolved Item (URI) is associated with the licensee's actions following a repair to
    The inspectors observed radiation worker performance with respect to stated RP work
ESW underground piping in the spring of 2009. The licensee conducted only a leak test
    requirements. The inspectors assessed whether workers were aware of the radiological
of the repairs rather than a hydrostatic test, and the coupling used to repair the pipe leak was not hydrostatically tested for 10 minutes prior to installation in the system. After further review of the repair process and interaction with the ASME code committee, the  
    conditions in their workplace and the RWP controls/limits in place, and whether their
inspectors determined that the Dresser coupling used to repair the pipe did not meet the  
    performance reflected the level of radiological hazards present.
ASME code definition of a 'component,' and was therefore not required to be
    The inspectors reviewed a maximum of 10 radiological problem reports since the last
hydrostatically tested. This URI is closed and no further actions are required.  
    inspection that found the cause of the event to be human performance errors. The
.2 Institute of Nuclear Power Operations Plant Assessment Report Review
    inspectors evaluated whether there was an observable pattern traceable to a similar
    cause. The inspectors assessed whether this perspective matched the corrective action
    approach taken by the licensee to resolve the reported problems. The inspectors
    discussed with the RP manager any problems with the corrective actions planned or
    taken.
  b. Findings
    No findings were identified.
.7  Radiation Protection Technician Proficiency (02.08)
   a. Inspection Scope
   a. Inspection Scope
  The inspectors reviewed the final report for the Institute of Nuclear Power Operations (INPO) plant assessment of Perry station conducted in August 2009. The inspectors
    The inspectors observed the performance of the RP technicians with respect to all RP
    work requirements. The inspectors evaluated whether technicians were aware of the
    radiological conditions in their workplace and the RWP controls/limits, and whether their
    performance was consistent with their training and qualifications with respect to the
    radiological hazards and work activities.
                                                  16                                  Enclosure


reviewed the report to ensure that issues
      The inspectors reviewed a maximum of 10 radiological problem reports since the last
identified were consistent with the NRC perspectives of licensee performance and to verify whether any significant safety issues were identified that required further NRC follow-up.
      inspection that found the cause of the event to be RP technician error. The inspectors
      evaluated whether there was an observable pattern traceable to a similar cause. The
      inspectors assessed whether this perspective matched the corrective action approach
      taken by the licensee to resolve the reported problems.
  b. Findings
      No findings were identified.
2RS3 In-Plant Airborne Radioactivity Control and Mitigation (71124.03)
      The inspection activities supplement those documented in IR 05000440/2010003, and
      constitute one complete sample as defined in IP 71124.03-05.
.1  Inspection Planning (02.01)
  a. Inspection Scope
      The inspectors reviewed the plant USAR to identify areas of the plant designed as
      potential airborne radiation areas and any associated ventilation systems or airborne
      monitoring instrumentation. Instrumentation review included continuous air monitors
      (continuous air monitors and particulate-iodine-noble-gas-type instruments) used to
      identify changing airborne radiological conditions such that actions to prevent an
      overexposure may be taken. The review included an overview of the respiratory
      protection program and a description of the types of devices used.
      The inspectors reviewed USAR, TS, and emergency planning documents to identify
      location and quantity of respiratory protection devices stored for emergency use.
      The inspectors reviewed the licensees procedures for maintenance, inspection, and use
      of respiratory protection equipment including self-contained breathing apparatus
      (SCBA). Additionally, the inspectors reviewed procedures for air quality maintenance
      and the reported PIs to identify any related to unintended dose resulting from intakes of
      radioactive materials.
  b. Findings
      No findings were identified.
.2  Engineering Controls (02.02)
  a. Inspection Scope
      The inspectors reviewed the licensees use of permanent and temporary ventilation to
      determine whether the licensee used ventilation systems as part of its engineering
      controls (in lieu of respiratory protection devices) to control airborne radioactivity. The
      inspectors reviewed procedural guidance for use of installed plant systems, such as
      containment purge, spent fuel pool ventilation, and auxiliary building ventilation, and
      assessed whether the systems are used, to the extent practicable, during high-risk
      activities (e.g., using containment purge during cavity flood up).
                                                    17                                    Enclosure


b. Findings
    The inspectors selected installed ventilation systems used to mitigate the potential for
  No findings of significance were identified.  
    airborne radioactivity, and evaluated whether the ventilation airflow capacity, flow path
    
    (including the alignment of the suction and discharges), and filter/charcoal unit
   28 Enclosure 4OA6 Meetings
    efficiencies, as appropriate, were consistent with maintaining concentrations of airborne
.1 Exit Meeting
    radioactivity in work areas below the concentrations of an airborne area to the extent
The inspectors presented the inspection results to the Site Vice-President, Mr. Mark Bezilla, and other members of licensee management on October 6, 2010. The inspectors asked the licensee whether any materials examined during the  
    practicable.
inspection should be considered proprietary. No proprietary information was identified. .2 Interim Exit Meetings
    The inspectors selected temporary ventilation system setups (HEPA/charcoal negative
An interim exit meeting was conducted for  
    pressure units, down draft tables, tents, metal Kelly buildings, and other enclosures)
radiological hazard assessment and exposure controls, in-plant airborne radioactivity control and mitigation, and occupational dose
    used to support work in contaminated areas. The inspectors assessed whether the use
assessment with Mr. T. Jardine and other members of the Perry staff
    of these systems was consistent with licensee procedural guidance and as-low-as-is-
on July 16, 2010. The inspectors confirmed that none of the potential report input discussed was
    reasonably-achievable (ALARA) concepts.
considered proprietary. 4OA7 Licensee-Identified Violations
  b. Findings
The following violation of very low safety significance (Green) was identified by the licensee and is a violation of NRC requirements which meets the criteria of the NRC
    No findings were identified.
Enforcement Policy, for being dispositioned as an NCV. On August 25, 2010, the licensee identified a failure to meet the requirements of TS 5.5.9, Diesel Fuel Oil Testing Program requirements by failing to conduct the test for viscosity at the prescribed temperature when receiving new fuel oil. The cause was
.3   Use of Respiratory Protection Devices (02.03)
a failure to make appropriate procedure changes when the site implemented a license change request that revised this TS requirement. Specifically, in September 1990, when the license change request was implemented by the site, the  
   a. Inspection Scope
temperature specified in SR 3.8.3.3 changed from 100 °F to 40 °C.  Following this
    For those situations where it is impractical to employ engineering controls to minimize
change, the site did not recognize that the fuel oil viscosity test procedures
    airborne radioactivity, the inspectors assessed whether the licensee provided respiratory
containing the prescribed testing temperature needed to be changed to align with the new TS requirements, and therefore, the procedures incorrectly continued to reflect the temperature cited in the previous TS version. Licensee personnel had been
    protective devices such that occupational doses are ALARA. The inspectors selected
testing the fuel oil in accordance with these procedures for approximately 20 years. Corrective actions include sampling of all three fuel storage tanks for the diesel generators, testing the samples for viscosity at the correct temperature requirement, and implementation of procedural changes to incorporate the revised temperature. All other TS-required surveillances of fuel oil properties were properly performed and  
    work activities where respiratory protection devices were used to limit the intake of
completed as required to ensure current operability. The violation was determined to  
    radioactive materials, and assessed whether the licensee performed an evaluation
be of low safety significance through a licensee evaluation of risk.  The licensee  
    concluding that further engineering controls were not practical and that the use of
entered this performance deficiency into the CAP as CR 10-81724, Fuel Oil Samples
    respirators was ALARA. The inspectors also evaluated whether the licensee had
Not Analyzed per Tech Specs. ATTACHMENT:  SUPPLEMENTAL INFORMATION 
    established means (such as routine bioassay) to determine if the level of protection
1 Attachment SUPPLEMENTAL INFORMATION KEY POINTS OF CONTACT
    (protection factor) provided by the respiratory protection devices during use was at least
Licensee 
    as good as that assumed in the licensees work controls and dose assessment.
M. Bezilla, Vice President Nuclear D. Evans, Work and Outage Management Director J. Grabnar, Site Engineering Director
    The inspectors assessed whether respiratory protection devices used to limit the intake
H. Hanson, Performance Improvement Director
    of radioactive materials were certified by the National Institute for Occupational Safety
T. Jardine, Operations Manager
    and Health/Mine Safety and Health Administration (NIOSH/MSHA) or have been
    approved by the NRC in accordance with 10 CFR 20.1703(b). The inspectors selected
    work activities where respiratory protection devices were used. The inspectors
    evaluated whether the devices were used consistent with their NIOSH/MSHA
    certification or any conditions of their NRC approval.
    The inspectors reviewed records of air testing for supplied-air devices and SCBA bottles
    to assess whether the air used in these devices meets or exceeds Grade D quality. The
    inspectors reviewed plant breathing air supply systems to determine whether they meet
    the minimum pressure and airflow requirements for the devices in use.
    The inspectors selected individuals qualified to use respiratory protection devices, and
    assessed whether they have been deemed fit to use the devices by a physician.
    The inspectors selected several individuals assigned to wear a respiratory protection
    device and observed them donning, doffing, and functionally checking the device as
    appropriate. Through interviews with these individuals, the inspectors evaluated
    whether they knew how to safely use the device and how to properly respond to any
                                                  18                                  Enclosure
 
    device malfunction or unusual occurrence (loss of power, loss of air, etc.). The
    inspectors reviewed training curricula for users of the devices.
    The inspectors chose various respiratory protection devices staged and ready for use in
    the plant or stocked for issuance. The inspectors assessed the physical condition of the
    device components (mask or hood, harnesses, air lines, regulators, air bottles, etc.) and
    reviewed records of routine inspection for each. The inspectors selected several of the
    devices and reviewed records of maintenance on the vital components (e.g., pressure
    regulators, inhalation/exhalation valves, hose couplings). The inspectors assessed
    whether onsite personnel assigned to repair vital components had received vendor-
    provided training.
  b. Findings
    No findings were identified.
.4  Self-Contained Breathing Apparatus for Emergency Use (02.04)
  a. Inspection Scope
    Based on USAR, TS, and emergency operating procedure requirements, the inspectors
    reviewed the status and surveillance records of SCBAs staged in-plant for use during
    emergencies. The inspectors reviewed the licensees capability for refilling and
    transporting SCBA air bottles to and from the control room and operations support
    center during emergency conditions.
    The inspectors selected individuals on control room shift crews, and individuals from
    designated departments currently assigned emergency duties (e.g., onsite search and
    rescue duties) to assess whether control room operators and other emergency response
    and RP personnel (assigned in-plant search and rescue duties or as required by
    emergency operating procedures or the emergency plan) were trained and qualified in
    the use of SCBAs (including personal bottle change out). The inspectors evaluated
    whether personnel assigned to refill bottles were trained and qualified for that task.
    The inspectors determined whether appropriate mask sizes and types were available for
    use (i.e., in-field mask size and type matched what was used in fit-testing). The
    inspectors selected various on-shift operators to determine whether they have no facial
    hair that would interfere with the sealing of the mask to the face and whether vision
    correction (e.g., glasses inserts or corrected lenses) were available as appropriate.
    The inspectors reviewed the past 2 years of maintenance records for several SCBA
    units used to support operator activities during accident conditions and designated as
    ready for service to assess whether any maintenance or repairs on any SCBA units
    vital components were performed by an individual, or individuals, certified by the
    manufacturer of the device to perform the work. The vital components typically are the
    pressure-demand air regulator and the low-pressure alarm. The inspectors reviewed the
    onsite maintenance procedures governing vital component work to determine any
    inconsistencies with the SCBA manufacturers recommended practices. For those
    SCBAs designated as ready for service, the inspectors determined whether the
    required, periodic air cylinder hydrostatic testing was documented and up to date, and
    the retest air cylinder markings required by the U.S. Department of Transportation were
    in place.
                                                  19                                  Enclosure
 
    b. Findings
      No findings were identified.
  .5  Problem identification and Resolution (02.05)
    a. Inspection Scope
      The inspectors reviewed CRs and other corrective action documents to determine
      whether problems associated with control and mitigation of in-plant airborne radioactivity
      were being identified at the appropriate threshold and were properly addressed for
      resolution in the licensees CAP.
    b. Findings
      No findings were identified
2RS4 Occupational Dose Assessment (71124.04)
      This inspection constituted a partial sample as defined in IP 71124.04-05.
  .1    Inspection Planning (02.01)
    a. Inspection Scope
      The inspectors reviewed the results of RP program audits related to internal and external
      dosimetry (e.g., licensees quality assurance audits, self-assessments, or other
      independent audits) to gain insights into overall licensee performance in the area of dose
      assessment and focus the inspection activities consistent with the principle of smart
      sampling.
    b. Findings
      No findings were identified.
  .2    Internal Dosimetry (02.03)
      Internal Dose Assessment - Airborne Monitoring
    a. Inspection Scope
      The inspectors reviewed the licensee's program for airborne radioactivity assessment
      and dose assessment, as applicable, based on airborne monitoring and calculations of
      derived air concentration. The inspectors determined whether flow rates and collection
      times for air sampling equipment were adequate to allow lower limits of detection to be
      obtained. The inspectors also reviewed the adequacy of procedural guidance to assess
      internal dose if respiratory protection was used. The licensee had not performed dose
      assessments using airborne/derived air concentration monitoring since the last
      inspection.
                                                    20                                  Enclosure


K. Krueger, Plant General Manager P. McNulty, Radiation Protection Manager M. Stevens, Maintenance Director
    b. Findings
J. Tufts, Chemistry Manager
        No findings were identified.
.3    Special Dosimetric Situations (02.04)
        Dosimeter Placement and Assessment of Effective Dose Equivalent for External
        Exposures.
    a.  Inspection Scope
        The inspectors reviewed the licensee's methodology for monitoring external dose in
        non-uniform radiation fields or where large dose gradients exist. The inspectors
        evaluated the licensee's criteria for determining when alternate monitoring, such as use
        of multi-badging, was to be implemented.
        The inspectors reviewed dose assessments performed using multi-badging to evaluate
        whether the assessment was performed consistent with licensee procedures and
        dosimetric standards.
    b. Findings
        No findings were identified.
4.      OTHER ACTIVITIES
4OA1 Performance Indicator Verification (71151)
  .1  Mitigating Systems Performance Index - Heat Removal System
    a.  Inspection Scope
        The inspectors sampled licensee submittals for the Mitigating Systems Performance
        Index (MSPI) - Heat Removal System performance indicator for the period from the third
        quarter 2009 through the second quarter 2010. To determine the accuracy of the PI
        data reported during those periods, PI definitions and guidance contained in the Nuclear
        Energy Institute (NEI) Document 99-02, Regulatory Assessment Performance Indicator
        Guideline, Revision 6, dated October 2009, were used. The inspectors reviewed the
        licensees operator narrative logs, issue reports, event reports, MSPI derivation reports,
        and NRC Integrated Inspection Reports for the period of the third quarter 2009 through
        the second quarter 2010 to validate the accuracy of the submittals. The inspectors
        reviewed the MSPI component risk coefficient to determine if it had changed by more
        than 25 percent in value since the previous inspection, and if so, that the change was in
        accordance with applicable NEI guidance. The inspectors also reviewed the licensees
        issue report database to determine if any problems had been identified with the PI data
        collected or transmitted for this indicator and none were identified. Documents reviewed
        are listed in the Attachment to this report.
        This inspection constituted one MSPI heat removal system sample as defined in
        IP 71151-05.
                                                      21                                Enclosure


   
  b. Findings
Other  C. O'Clare, Ohio Department of Health
    No findings of significance were identified.
   
.2 Mitigating Systems Performance Index - Residual Heat Removal System
  LIST OF ITEMS OPENED, CLOSED AND DISCUSSED
  a. Inspection Scope
Opened and Closed
    The inspectors sampled licensee submittals for the MSPI - Residual Heat Removal
05000440/2010004-01 NCV Unacceptable Preconditioning of RHR Valve Prior to ASME In-Service Testing (1R22) 05000440/2010004-02 NCV Failure to Comply with Technical Specification LCOs When
    System performance indicator for the period from the third quarter 2009 through the
Reactor Vessel Level Instruments Were Declared
    second quarter 2010. To determine the accuracy of the PI data reported during those
Inoperable (4OA2.4)
    periods, PI definitions and guidance contained in the Nuclear Energy Institute (NEI)
    Document 99-02, Regulatory Assessment Performance Indicator Guideline,
Closed 05000440/2010003-06 URI Failure to Hydrostatically Test Replacement Components in Accordance with ASME (Section 4OA5.1) 05000440/2010-003 LER Loss of Control Rod Drive Header Pressure Results in
    Revision 6, dated October 2009, were used. The inspectors reviewed the licensees
Manual RPS Actuation (Section 4OA3.1)
    operator narrative logs, issue reports, MSPI derivation reports, event reports and NRC
    Integrated Inspection Reports for the period of the third quarter 2009 through the second
Discussed 45815 EN Retraction of Event Notification 45815:  Loss of Safety Function to Control the Release of Radioactive Material (Section 4OA3.2) 
    quarter 2010 to validate the accuracy of the submittals. The inspectors reviewed the
2 Attachment LIST OF DOCUMENTS REVIEWED The following is a partial list of documents reviewed during the inspection.  Inclusion on this list does not imply that the NRC inspector reviewed the documents in their entirety, but rather that
    MSPI component risk coefficient to determine if it had changed by more than 25 percent
selected sections or portions of the documents were evaluated as part of the overall inspection effort. Inclusion of a document on this list does not imply NRC acceptance of the document or any part of it, unless this is stated in the body of the inspection report.  
    in value since the previous inspection, and if so, that the change was in accordance with
    applicable NEI guidance. The inspectors also reviewed the licensees issue report
1R01 Adverse Weather
    database to determine if any problems had been identified with the PI data collected or
 
    transmitted for this indicator and none were identified. Documents reviewed are listed in
CR 10-80444; Security Project - North-Side Concrete 'T' Wall Installation Issues Drawing 743-0013-00000; Topography and Storm Drain Composite; Revision D EER 600631290; Perform Evaluation to Determine Locations of Drainage Gaps in Installed T-Walls; dated August 4, 2010 1R04 Equipment Alignment
    the Attachment to this report.
 
    This inspection constituted one MSPI residual heat removal system sample as defined in
CR 08-42257; Annulus Exhaust Gas Treatment
    IP 71151-05.
System (AGETS) "A" Train Low Flow Adjustment; dated June 20, 2008 CR 10-72614; Unplanned Fire Suppression Impair
b. Findings
ment for Annulus Exhaust Gas Treatment System; dated March 4, 2010 CR 08-34483; Annulus Exhaust Gas Treatment System Flow Indication Low Flow; dated
    No findings of significance were identified.
January 29, 2008 CR 07-31871; AEGTS B Discharge Damper Is Not Functioning Correctly; dated December 21, 2007 Drawing 912-0605-00000; Reactor Building Annulus Exhaust Gas Treatment; Revision W PYBP-POS-2-2; Annulus Exhaust Gas Treatment System A (B) Outage Protected Equipment
.2 Mitigating Systems Performance Index - Cooling Water Systems
Posting Checklist; Revision 10 PNPP No. 10392; Annulus Exhaust Gas Treatment System A (B) Outage Protected Equipment Posting Checklist; dated July 14, 2009  SOI-M15; AEGTS System; Revision 8 VLI-M23/24; MCC, Switchgear and Miscellaneous Electrical Equipment Area HVAC System;
a. Inspection Scope
Revision 7 CR 10-82114; 0M23C0002B Did Not Trip with a B Train Trip Signal Present; dated September 2, 2010 CR 10-82118; Replacement Solenoid Valve Mount Screw Holes Are Not Threaded; dated August 31, 2010 Drawing 912-0609-00000; MCC Switchgear and Misc Electrical Equipment Areas HVAC System and Battery Room Exhaust; Revision AA Perry Plant Health Report 2010-2 for P42 - Emergency Closed Cooling System
    The inspectors sampled licensee submittals for the MSPI - Cooling Water Systems
SOI-P42; Emergency Closed Cooling System; Revision 16 VLI-P42; Emergency Closed Cooling System; Revision 15 Drawing 302-0621-00000; Emergency Closed Cooling System; Revision SS
    performance indicator for the period from the third quarter 2009 through the second
Drawing 208-0041-00002; Reactor Protection System MG Set S001B
    quarter 2010. To determine the accuracy of the PI data reported during those periods,
Drawing 208-0041-00001; Reactor Protection System MG Set S001A CR 10-81707; Overheating on Voltage Regulator for RPS MG Set B; dated August 25, 2010 
    PI definitions and guidance contained in the NEI Document 99-02, Regulatory
3 Attachment 1R05 Fire Protection (Annual/Quarterly)
    Assessment Performance Indicator Guideline, Revision 6, dated October 2009, were
 
    used. The inspectors reviewed the licensees operator narrative logs, issue reports,
PAP-1910; Fire Protection Program; Revision 19 P54-24; Calculation of Combustible Loading and Allowable Limits for Fire Loading; Revision 4 FPI-0IB; Pre-Fire Plan Instruction - Intermediate Building; Revision 5
    MSPI derivation reports, event reports and NRC Integrated Inspection Reports for the
FPI-0CC; Pre-Fire Plan Instruction - Control Complex; Revision 8
    period of the third quarter 2009 through the second quarter 2010 to validate the
CR 10-80981; Documentation of NRC Questions; dated August 9, 2010
    accuracy of the submittals. The inspectors reviewed the MSPI component risk
CR 10-81985; Response to Questions from the NRC Resident Inspector; dated August 27, 2010 FPI-1AB; Pre-Fire Plan Instruction - Auxiliary Building; Revision 3 CR 10-82504; NRC Question Regarding Pen Seals in AX 620' West; dated September 10, 2010
    coefficient to determine if it had changed by more than 25 percent in value since the
    previous inspection, and if so, that the change was in accordance with applicable NEI
1R06 Internal Flooding
    guidance. The inspectors also reviewed the licensees issue report database to
 
    determine if any problems had been identified with the PI data collected or transmitted
PAP-0204; Housekeeping/Cleanliness Control Program; Revision 24 ARI-H13-P601-0018; Leak Detection; Revision 13 NOP-OP-1012; Material Readiness and Housekeeping Inspection Program; Revision 5
    for this indicator and none were identified. Documents reviewed are listed in the
CR 10-77685; Various Through Wall Piping Leaks on N71; dated June 3, 2010 Drawing 911-0617; Auxiliary Building Drains; Revision F 1R11 Licensed Operator Requalification Program
    Attachment to this report.
 
                                                22                                  Enclosure
PYBP-PTS-0005; Operator Continuing Training Program Administration; Revision 25 PYBP-POS-0027; Operator Actions from Memory; Revision 0, dated December 3, 2008  Simulator Exercise Guide OTLC-3058201010_PY_SGC1; Cycle 10 2010 Evaluated Scenario
C1; Revision 0 CR 10-80980; Unsat Training Observation - Ops Performance Improvement Time Not Properly Used; dated August 9, 2010 CR 10-81725; Unqualified Individuals Signing as Training Coordinators; dated August 25, 2010 1R12 Maintenance Effectiveness
  WO 200284303; Chg Oil Fltrs Combustion Gas Purge Unit; dated July 21, 2010
CR 10-79817; Wrong Oil Added to CGMC Reservoir; dated July 17, 2010
CR 10-80089; NRC-ID. No FME High Risk Brief Sheet in Work Order; dated July 22, 2010
CR 10-80169; Failed PMT for CGMC B Aux Oil Pump; dated July 24, 2010
Clearance EPY-M25-0005; Control Room HVAC Supply Plenum; dated September 1, 2010 LCOTR# A10-M25-032; M25/26 Inoperable, Period 5 Week 10; dated August 30, 2010 CR 10-81952; Relay Contacts do not Change State; dated August 30, 2010
CR 10-81957; Loose Fittings on Low Flow Switch; dated August 30, 2010


Drawing 912-0610-00000; Control Room HVAC
      This inspection constituted one MSPI cooling water system sample as defined in
  and Emergency Recirculation System;
      IP 71151-05.
Revision FF CR 10-82639; Maintenance HPCS Work Start Deficiencies; dated September 13, 2010 CR 10-82715; Inadequate Order for Div 3 Fuel Oil Day Tank Work; dated September 16, 2010
  b. Findings
CR 10-82864; Grease Fitting Damaged during Disassembly; dated September 19, 2010
      No findings of significance were identified.
CR 10-82970; Less Than Adequate Contingency Planning for Div 3 DG Inspections; dated September 21, 2010 CR 10-82989; FME Concerns Identified in Div 3 DG Room; dated September 20, 2010 CR 10-83194; PMT Could Not Be Worked as Written; dated September 24, 2010
4OA2 Problem Identification and Resolution (71152)
WO 200430281; Rebuild Ball Valves to Small and Large Seals
      Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency
CR 10-83134; Lower Airlock Door Air Supply Flex Hoses Possibly Defective
      Preparedness, Public Radiation Safety, Occupational Radiation Safety, and
CR 10-82842; Lower Airlock Pneumatic System Pressure Drop Test Failed 
      Physical Protection
4 Attachment CR 10-76252; Lower Containment Airlock Reactor Door CR 09-69338; Upper Containment Airlock Reactor Door
.1  Routine Review of Items Entered Into the CAP
  a. Inspection Scope
      As part of the various baseline inspection procedures discussed in previous sections of
      this report, the inspectors routinely reviewed issues during baseline inspection activities
      and plant status reviews to verify that they were being entered into the licensees CAP at
      an appropriate threshold, that adequate attention was being given to timely corrective
      actions, and that adverse trends were identified and addressed. Attributes reviewed
      included: identification of the problem was complete and accurate; timeliness was
      commensurate with the safety significance; evaluation and disposition of performance
      issues, generic implications, common causes, contributing factors, root causes,
      extent-of-condition reviews, and previous occurrences reviews were proper and
      adequate; and that the classification, prioritization, focus, and timeliness of corrective
      actions were commensurate with safety and sufficient to prevent recurrence of the issue.
      Minor issues entered into the licensees CAP as a result of the inspectors observations
      are included in the Attachment to this report.
      These routine reviews for the identification and resolution of problems did not constitute
      any additional inspection samples. Instead, by procedure they were considered an
      integral part of the inspections performed during the quarter and documented in
      Section 1 of this report.
  b. Findings
      No findings were identified.
.2  Daily Corrective Action Program Reviews
  a. Inspection Scope
      In order to assist with the identification of repetitive equipment failures and specific
      human performance issues for follow-up, the inspectors performed a daily screening of
      items entered into the licensees CAP. This review was accomplished through
      inspection of the stations daily CR packages.
      These daily reviews were performed by procedure as part of the inspectors daily plant
      status monitoring activities and, as such, did not constitute any separate inspection
      samples.
                                                      23                                  Enclosure


1R13 Maintenance Risk Assessments and Emergent Work Control
  b. Findings
 
    No findings were identified.
NOP-OP-1007; Risk Management; Revision 7
.3  Semi-Annual Trend Review
CR 10-80396; Perry Not Notified of Conservative Grid Ops; dated July 28, 2010
  a. Inspection Scope
CR 10-81724; Finding - Fuel Oil Samples not Analyzed per Tech Specs; dated August 25, 2010
    The inspectors performed a review of the licensees CAP and associated documents to
CR 10-81727; Diesel Fuel Oil Sample Analysis Completion Dates Inconsistent; dated August
    identify trends that could indicate the existence of a more significant safety issue. The
25, 2010 CR 10-81733; Procedure Steps Signed as Performed Inappropriately; dated August 25, 2010
    inspectors review was focused on repetitive equipment issues, but also considered the
CR 10-82658; Water/Steam Leak From 1N27F505D (RFBP D Discharge Check Valve); dated September 15, 2010 WO 200430709; Wire Wrap/Inject Inspection Flange; dated September 17, 2010 WO 200430710; Remove Insulation @ Valve; dated September 16, 2010 ECP 10-0570-000; Leak Sealant Device on Reactor Feedwater Booster Pump 'D' Discharge
    results of daily inspector CAP item screening discussed in Section 4OA2.2 above,
Check Valve (1N27F0505D); Revision 0 ECP 10-0570-001; Install and Inject Leak Sealant Device on Reactor Feedwater Booster Pump 'D' Discharge Check Valve (1N27F0505D); Revision 1 CR 10-82682; Div 3 DG Generator Inter Pole Side Plate Movement; dated September 15, 2010 CR 10-82992; Div 3 Diesel Generator - Migrating Exciter Field Core Plates; dated September 22, 2010
    licensee trending efforts, and licensee human performance results. The inspectors
WO 200430766; Remove Generator Rotor, Inspect for Loose Wedge Studs; dated September 15, 2010 1R15 Operability Evaluations
    review nominally considered the 6-month period from January 2010 through June 2010,
 
    although some examples expanded beyond those dates where the scope of the trend
CR 10-78672; 1M43 Agastat Relay Qualification Issue; dated June 22, 2010 CR 10-81023; M52 Turning Vanes Degraded; dated August 10, 2010 Prompt Functionality Assessment for Degraded TSC Ventilation Supply Fan Turning Vanes; dated August 13, 2010 Prompt Operability Determination for Diesel Generator Building Ventilation Systems; dated
    warranted.
July 15, 2010 CR 10-81973; No Insulation Inside Plenum; dated August 30, 2010
    The reviews also included issues documented outside of the normal CAP in major
eSOMS Narrative Logs dated September 2, 2010
    equipment problem lists, repetitive and/or rework maintenance lists, departmental
Prompt Operability Determination for ECC to  
    problem/challenges lists, system health reports, quality assurance audit/surveillance
FPCC Heat Exchanger Bypass Valve Stroke Time
    reports, self-assessment reports, and maintenance rule assessments. The inspectors
Testing Failure; August 24, 2010 CR 10-81623; OP42F0255B Failed Stroke Closed Test; dated August 23, 2010
    compared and contrasted their results with the results contained in the licensees
    CAP trending reports. Corrective actions associated with a sample of the issues
    identified in the licensees trending reports were reviewed for adequacy.
    This review constituted a single semi-annual trend inspection sample as defined in
    IP 71152-05.
  b. Findings
    No findings were identified.
.4  In-depth Review- Technical Specifications Compliance
  a. Inspection Scope
    The inspectors performed an annual follow-up of selected issues sample of the
    licensees process for performing and documenting TS compliance. The inspectors
    reviewed documentation in the licensees CAP, official narrative operating logs and LCO
    tracking module, for compliance with site-specific administrative, operational, and
    licensing procedures specifically to assess for proper control and documentation of the
    entry and exit of LCO Conditions and Required Actions. Documents reviewed are listed
    in the Attachment to this report.
    This review constituted one in-depth problem identification and resolution sample as
    defined in IP 71152-05.
  b. Findings
    Introduction: The inspectors identified a finding of very low safety significance (Green)
    and an associated NCV for the licensees failure to follow the requirements of TS
    LCO 3.0.2 by not entering TS LCO 3.3.5.1 Condition A and TS 3.3.6.1 Condition A when
                                                  24                                   Enclosure


1R18 Permanent/Temporary Modifications
reactor vessel level instruments 1B21N0673C and 1B21N0674C were declared
 
inoperable. Technical Specification LCO 3.0.2 requires that Upon discovery of a failure
Perry Plant Health Report 2010-2 for Temporary Modifications
to meet an LCO, the Required Actions of the associated Conditions shall be met, except
NOP-CC-2003; Engineering Changes; Revision 14
as provided in LCO 3.0.5 and LCO 3.0.6.
NORM-CC-2001; Engineering Change Process Flowcharts; Revision 00 ECP 10-0020-0000; Reference Documents - Hot Surge Tank Low Level Alarm from Level Transmitter Signal; Revision 0 ECP 10-0020-0001; Hot Surge Tank Low Level Alarm from Level Transmitter Signal; Revision 3  
Description: On August 9, 2010, during a review of operator narrative logs, the
WO 200399695; Hot Surge Tank Low Level Alarm; dated May 15, 2010  
inspectors noted a log entry that identified the use of a TS Surveillance Requirement
NOBP-ER-3003-01; Temporary Modification Review Checklist; Revision 00 CR 09-67788; Host Surge Tank (HST) Level Low Alarm Locked In; dated November 15, 2009
(SR) Note to support the performance of WO #200322765, PDP - New PM Replace
Drawing 302-0081-00000; Feedwater; Revision BBB 
Rosemount STU Card. This WO included a step to acquire as-found data of the card
5 Attachment
being replaced prior to its removal. The method of acquiring this as-found data included
Drawing 302-0101-00000; Condensate System; Revision TT
performing portions of surveillance test procedure SVI-B21-T0187C, ECCS/HPCS RPV
Drawing 208-0149-00002; MDFP Auto Start Logic & RFBP Auto Start Logic; Revision S
Water Level 2 and Level 8 Channel C Functional for 1B21-N673C. Additionally, this WO
CR 10-82802; Potential Single Failure Vulnerability with Hot Surge Tank Temp Mod; dated September 16, 2010 1R19 Post-Maintenance Testing
step stated, Sign Off/Close Surveillance Instruction as No Credit. Surveillance test
  SVI-B21-T0137F; ECCS Drywell Pressure High Channel "F" Functional for 1B21-N694F;
SVI-B21-T0187C renders Reactor Vessel Level instruments 1B21N0673C and
Revision 5 PTI-M23-P0005; Emergency Service Water Pump
1B21N0674C inoperable. This surveillance references the TS Surveillance Notes
House Ventilation System Train B Damper  Stroking; Revision 5 WO 200323496; Replace Rosemount MTU Card; dated August 11, 2010 WO 200323644; Replace Keylock Control Switch 1B21C-S27A; dated August 4, 2010
associated with SR 3.3.5.1 and 3.3.6.1. These SR Notes state, in part, When a channel
WO 200340398; Replace and Perform Calibration Check of 1M15D0001B Instrumentation; dated August 25, 2010 WO 200327715; Replace AEGT Fan 'B' Motor; dated August 25, 2010
is placed in an inoperable status solely for performance of required Surveillances, entry
WO 200290571; Replace SLS/MTR/Oil Hydramotor at ESW "B" Outlet Damper; dated September 6, 2010 WO 200333304; MERP - Replace Utility Station w/NUS; dated September 6, 2010
into associated Conditions and Required Actions may be delayed. The licensee utilized
CR 10-81632; Temperature Switch Found Tripped; dated August 23, 2010
the SR Note during the performance of as-found checks using the surveillance and did
CR 10-81633; RFACR: Damaged Field Conductor to Motor; dated August 23, 2010
not enter the Conditions and Required Actions for the 22 minutes it took to perform the
WO 200328863; Replace Cntrl Relays in EH1304 Cubicle; dated September 20, 2010 SOI-R22; Metal Clad Switchgear 5-15 KV; Revision 25 CR 10-82852; Unexpected Reading Obtained during Functional Testing; dated September 19, 2010 SVI-E22-T1319; Diesel Generator Start and Load Division 3; Revision 15
test.
CR 10-83148; Div 3 Emergency Diesel Generator Failure to Start During Testing; dated September 24, 2010 CR 10-83163; Generator Stator Temperature Monitor is Erratic and Unreliable; dated September 24, 2010 CR 10-83181; Div 3 DG Additional Tagging Points Requested; dated September 24, 2010
The inspectors reviewed the licensees use of the surveillance notes and determined
that the delay in entering the Conditions and Required Actions was inappropriate
because the surveillance was being performed to satisfy WO requirements, not
TS-required SRs. As a result, the licensee declared the instruments inoperable but
did not enter the Conditions or Required Actions for the associated LCOs. This is
contrary to the requirements of TS LCO 3.0.2 which states Upon discovery of a failure
to meet an LCO, the Required Actions of the associated Conditions shall be met, except
as provided in LCO 3.0.5 and LCO 3.0.6. Limiting Condition of Operation 3.0.5 and
LCO 3.0.6 did not apply in this situation.
An additional review of recent narrative log entries identified several instances of
misapplication of the same surveillance notes. The longest time period the LCO was not
adhered to was 4 hours and 47 minutes. In combination with the replacement and
subsequent operability testing, the instrument(s) were inoperable on several different
occasions, for a sum total of 13 hours and 29 minutes. The LCO allows the instrument(s)
to be inoperable for up to 24 hours before any additional actions are required. The
inspectors did not identify any instances where the LCO Required Action times were
exceeded.
Analysis: The inspectors determined that the licensees failure to follow TS LCO 3.0.2
constituted a performance deficiency. Specifically, the licensee did not enter the LCOs
and Required Actions for inoperable TS equipment. The inspectors evaluated the
performance deficiency in accordance with IMC 0612, Appendix B, Issue Screening.
This performance deficiency was not similar to any of the examples in IMC 0612,
Appendix E, Examples of Minor Issues," but was characterized as more than minor
because it impacted the Equipment Performance attribute of the Mitigating Systems
Cornerstone, and adversely affected the cornerstone objective to ensure the availability,
reliability, and capability of systems that respond to initiating events to prevent
undesirable consequences (i.e., core damage); and if left uncorrected it could lead to a
more significant safety concern.
                                              25                                  Enclosure


      The inspectors determined the finding could be evaluated using the SDP in accordance
1R22 Surveillance Testing
      with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 -
  SVI-E12-T2001; RHR A Pump and Valve Operability Test; Revision 26
      Initial Screening and Characterization of findings, Table 3b for the Mitigating Systems
SVI-E12-T1194; LPCI Pump A Discharge Low Flow (Bypass) Channel Functional for 1E12-N652A; Revision 8 SVI-E51-T2001; RCIC Pump and Valve Operability Test; Revision 32
      Cornerstone. The inspectors determined the finding was of very low safety significance
CR 01-79624; NRC-Identified Concern for Pre-conditioning Valve During Surveillance Testing;
      (Green) because it was not a design/qualification deficiency, did not represent a loss of
dated July 12, 2010 NOP-ER-3204; Inservice Testing Program; Revision 1
      system safety function, did not result in a loss of function of a single train for greater than
      its TS-allowable outage time, did not result in a loss of function of nonsafety-related
      risk-significant equipment and was not risk significant due to external events.
      This finding has a cross-cutting aspect in the decision making component of the Human
      Performance cross-cutting area (per IMC 0310 H.1(b)), because the licensee did not use
      conservative assumptions to ensure the proposed action was safe. Specifically, the
      licensee incorrectly used the TS SR Note to satisfy maintenance requirements.
      Enforcement: The inspectors determined that the finding represents a violation of
      regulatory requirements because it involved improper implementation of TS. The
      licensee utilized TS SR Notes while performing surveillances to satisfy maintenance
      WOs. In accordance with TS LCO 3.0.2, in these cases entry into TS LCO 3.3.5.1
      Condition A and 3.3.6.1 Condition A is required. Contrary to the above, the licensee did
      not enter the Conditions and Required Actions immediately upon declaring TS-required
      instrumentation inoperable. Because this finding is of very low safety significance and
      because it was entered into the licensees CAP as CR 10-81162, this violation is being
      treated as an NCV consistent with Section 2.3.2 of the NRC Enforcement Policy.
      (NCV 05000440/2010004-02; Failure to Comply with Technical Specification LCOs
      When Reactor Vessel Level Instruments Were Declared Inoperable.)
4OA3 Follow-up of Events and Notices of Enforcement Discretion (71153)
.1  (Closed) Licensee Event Report 05000440/2010-003: Loss of Control Rod Drive Header
      Pressure Results in Manual RPS Actuation
  a. Inspection Scope
      On May 11, 2010, a manual actuation of RPS was inserted to comply with TS because
      of multiple accumulators being inoperable coincident with the inability to restore control
      rod drive (CRD) charging header pressure. A trip unit failure caused an invalid
      loss-of-coolant accident (LOCA) initiation signal and resulted in the load shed of the
      XH12 stub bus. Due to an abnormal electrical lineup, both CRD pumps tripped and they
      were unable to be restarted. The licensee replaced the trip unit and restored the CRD
      system to its normal configuration. The licensee documented the failed equipment in
      CR 10-76727. The inspectors reviewed this Licensee Event Report (LER) and did not
      identify any findings or violations of NRC requirements. Documents reviewed as part of
      this inspection are listed in the attachment. This LER is closed.
      This event follow-up review constituted one sample as defined in IP 71153-05.
                                                    26                                    Enclosure


eSOMS Narrative Logs dated July 7-8, 2010  
.2  (Closed) Retraction of Event Notification 45815: Loss of Safety Function to Control the
SVI-P45-T2002; ESW Pump B and Valve Operability Test; Revision 26
      Release of Radioactive Material
SVI-R10-T5227; Off-Site Power Availability Verification; Revision 2
  a. Inspection Scope
      On April 6, 2010, the licensee initiated an event notification (EN) related to a loss of
      safety function involving five containment isolation valves. Specifically, the licensee
      reported that they had a potential loss of safety function for the ability to control the
      release of radioactive material. This was due to a loss of power to the LOCA isolation
      logic associated with containment penetration single valve isolations. On June 6, 2010,
      the licensee retracted this notification. The licensee evaluated the condition and
      determined the containment penetrations were still able to perform their design function.
      The inspectors reviewed the information contained in the evaluation, and did not identify
      any findings or violations related to the licensees retraction. This EN retraction is
      closed.
      This event follow-up review constituted one sample as defined in IP 71153-05.
4OA5 Other Activities
.1  (Closed) Unresolved Item 05000440/2010003-06: Failure to Perform a Hydrostatic Test
      in Accordance with ASME Code
  a. Inspection Scope
      This Unresolved Item (URI) is associated with the licensees actions following a repair to
      ESW underground piping in the spring of 2009. The licensee conducted only a leak test
      of the repairs rather than a hydrostatic test, and the coupling used to repair the pipe leak
      was not hydrostatically tested for 10 minutes prior to installation in the system. After
      further review of the repair process and interaction with the ASME code committee, the
      inspectors determined that the Dresser coupling used to repair the pipe did not meet the
      ASME code definition of a component, and was therefore not required to be
      hydrostatically tested. This URI is closed and no further actions are required.
.2  Institute of Nuclear Power Operations Plant Assessment Report Review
  a. Inspection Scope
      The inspectors reviewed the final report for the Institute of Nuclear Power Operations
      (INPO) plant assessment of Perry station conducted in August 2009. The inspectors
      reviewed the report to ensure that issues identified were consistent with the NRC
      perspectives of licensee performance and to verify whether any significant safety issues
      were identified that required further NRC follow-up.
  b. Findings
      No findings of significance were identified.
                                                    27                                    Enclosure


   
4OA6 Meetings
  6 Attachment 2RS1 Radiological Hazard Assessment and Exposure Controls
  .1  Exit Meeting
 
    The inspectors presented the inspection results to the Site Vice-President,
CR 09-56065; Containment Vessel Drywell Purge Degraded Flows Impacting Refuel Floor;
    Mr. Mark Bezilla, and other members of licensee management on October 6, 2010.
dated March 25, 2009 CR 09-57294; Boundary Exceeded Radiological Controlled Area (RCA); dated April 16, 2009 
    The inspectors asked the licensee whether any materials examined during the
CR 09-60436; Dose Rates in the P5480405 Condensate Backwash Receiving Tanl Higher than Expected; dated June 11, 2009 CR 09-62628; Radioactive Material Found Outside the RCA; dated August 2, 2009
    inspection should be considered proprietary. No proprietary information was identified.
CR 09-63398 and Associated Apparent Cause Evaluation; Platform Found Outside with Fixed Contamination; dated August 18, 2009 CR 09-66069; RISB Radioactive Material Inventory Discrepancies; dated October 16, 2009
.2 Interim Exit Meetings
CR 10-76774; Radiological Issues Associated with Division 2 ECC LOCA Initiation; dated May 11, 2010 CR-09-54403; RFO-12 Elevated Airborne Levels During Separator Lift; dated February 28, 2009 HPI-C0014; Radlock key Issue; Revision 01 HPI-H0004; Identification of Radioactive Materials and Release of Materials from RCAs;
    An interim exit meeting was conducted for radiological hazard assessment and exposure
Revision 22  HPI-K0009; Operation of the WARF, RISB and OSSC Yard; Revision 0
    controls, in-plant airborne radioactivity control and mitigation, and occupational dose
HPI-L0004; Source Control Documentation and Inventory; Revision 8 NOPB-NF-3102; Control of Non-Special Nuclear Material in the Fuel Pools; Revision 00 NOP-OP-4101; Access Controls for Radiologically Controlled Areas; Revision 01
    assessment with Mr. T. Jardine and other members of the Perry staff on July 16, 2010.
NOP-OP-4102; Radiological Postings, Labeling, and Markings; Revision 05
    The inspectors confirmed that none of the potential report input discussed was
NOP-OP-4107; Radiation Work Permit; Revisions 4 and 5
    considered proprietary.
NRC Form 748; National Source Tracking Transaction Report; dated January 12, 2009
4OA7 Licensee-Identified Violations
NSTS Annual Inventory Reconciliation; dated September 9, 2009, and January 29, 2010 PNPP No. 10280; Sealed Source Leak Test Data Sheet HPI-L0004; dated January 13, 2010 PNPP No. 7445; Sealed Source Leak Test Data Sheet ORM 6.4.2; dated January 13, 2010
    The following violation of very low safety significance (Green) was identified by the
SVI-E31-T5190; Sealed Source Leak Test and Inventory; Revision 5
    licensee and is a violation of NRC requirements which meets the criteria of the NRC
    Enforcement Policy, for being dispositioned as an NCV.
    *  On August 25, 2010, the licensee identified a failure to meet the requirements of TS
        5.5.9, Diesel Fuel Oil Testing Program requirements by failing to conduct the test for
        viscosity at the prescribed temperature when receiving new fuel oil. The cause was
        a failure to make appropriate procedure changes when the site implemented a
        license change request that revised this TS requirement. Specifically, in September
        1990, when the license change request was implemented by the site, the
        temperature specified in SR 3.8.3.3 changed from 100 °F to 40 °C. Following this
        change, the site did not recognize that the fuel oil viscosity test procedures
        containing the prescribed testing temperature needed to be changed to align with the
        new TS requirements, and therefore, the procedures incorrectly continued to reflect
        the temperature cited in the previous TS version. Licensee personnel had been
        testing the fuel oil in accordance with these procedures for approximately 20 years.
        Corrective actions include sampling of all three fuel storage tanks for the diesel
        generators, testing the samples for viscosity at the correct temperature requirement,
        and implementation of procedural changes to incorporate the revised temperature.
        All other TS-required surveillances of fuel oil properties were properly performed and
        completed as required to ensure current operability. The violation was determined to
        be of low safety significance through a licensee evaluation of risk. The licensee
        entered this performance deficiency into the CAP as CR 10-81724, Fuel Oil Samples
        Not Analyzed per Tech Specs.
ATTACHMENT: SUPPLEMENTAL INFORMATION
                                                  28                                  Enclosure


TEDE ALARA Evaluations for ALARA Plan Nos. 09-6018-02, 09-6041-00 and  
                              SUPPLEMENTAL INFORMATION
10-0066; dates October 2008 and February 2010 2RS3 In-Plant Airborne Radioactivity Control and Mitigation
                                KEY POINTS OF CONTACT
  Air Sample Records/Collection and Evaluation Forms for Various Work Activities and Locations; Various Dates in March and April 2009 CR 09-57025; Air Sampling Equipment Found with Expired Calibration; dated April 09, 2009
Licensee
EP-Emergency Plan for Perry Nuclear Power Plant Docket Nos. 50-440; Revision 30
M. Bezilla, Vice President Nuclear
HPI-G0007; Maintenance of Respiratory Protective Equipment and Operation of the Respirator Cleaning / Issue Facilities; Revision 21 HPI-G0008; Requalification of Respirators; Revision 07 HPI-L0003; Equipment History; Revision 06
D. Evans, Work and Outage Management Director
HRI-0003; Respirator Qualification Health Assessment; Revision 02  
J. Grabnar, Site Engineering Director
NOP-OP-4301; Respiratory Protection Program; Revision 01
H. Hanson, Performance Improvement Director
NOP-OP-4302; Issuing Respiratory Protection; Revision 00 NOP-OP-4303; Respirator Quantitative Fit Test Portacount PRO 8030; Revision 01 NOP-OP-4310; Firehawk M7 Self Contained Breathing Apparatus; Revision 04
T. Jardine, Operations Manager
NOP-OP-4702; Air Sampling; Revision 01
K. Krueger, Plant General Manager
PSI-0022; Emergency Plan Training program; Revision 03
P. McNulty, Radiation Protection Manager
PYBP-RPS-0038; Radiologically Controlled Area HEPA Ventilation and HEPA Vacuum Unit
M. Stevens, Maintenance Director
Program; Revision 01 
J. Tufts, Chemistry Manager
7 Attachment 2RS4 Occupational Dose Assessment
Other
 
C. OClare, Ohio Department of Health
ALARA Plan 09-6040; Suppression Pool Cleaning and Inspection; Revision 03 NOP-OP-4204; Special External Exposure Monitoring; Revision 03 NOP-OP-4204-04; Effective Dose Equivalent Dose Determination; Revision 01
                    LIST OF ITEMS OPENED, CLOSED AND DISCUSSED
NOP-OP-4205; Dose Assessment; Revision 03
Opened and Closed
NOP-OP-4206; Bioassay Program; Revision 00
05000440/2010004-01        NCV      Unacceptable Preconditioning of RHR Valve Prior to ASME
NOP-OP-4503; Personnel Contamination Monitoring; Revision 02
                                    In-Service Testing (1R22)
Radiological Engineering Assessment; Source te
05000440/2010004-02       NCV      Failure to Comply with Technical Specification LCOs When
rm Determination for Cycle 12 Operations;
                                    Reactor Vessel Level Instruments Were Declared
Undated RWP 09-6040; RFO-12 Suppression Pool Diving Activities; Revision 03
                                    Inoperable (4OA2.4)
Closed
05000440/2010003-06        URI      Failure to Hydrostatically Test Replacement Components in
                                    Accordance with ASME (Section 4OA5.1)
05000440/2010-003          LER      Loss of Control Rod Drive Header Pressure Results in
                                    Manual RPS Actuation (Section 4OA3.1)
Discussed
45815                      EN      Retraction of Event Notification 45815: Loss of Safety
                                    Function to Control the Release of Radioactive Material
                                    (Section 4OA3.2)
                                                    1                              Attachment


                                  LIST OF DOCUMENTS REVIEWED
4OA1 Performance Indicator Verification
The following is a partial list of documents reviewed during the inspection. Inclusion on this list
  NOBP-LP-4012; NRC Performance Indicators; Revision 3 NOBP-LP-4012-06; MSPI Data Sheets for Heat Removal System from July 2009 to June 2010;
does not imply that the NRC inspector reviewed the documents in their entirety, but rather that
Revision 2 NOBP-LP-4012-07; MSPI Data Sheets for Residual Heat Removal System from July 2009 to June 2010; Revision 2 NOBP-LP-4012-19; MSPI Data Sheets for Emergency Service Water from July 2009 to June 2010; Revision 2 Mitigating Systems Performance Index Basis Document; Revision 4  
selected sections or portions of the documents were evaluated as part of the overall inspection
PYBP-DES-0011; Mitigating Systems Performance Index; Revision 1
effort. Inclusion of a document on this list does not imply NRC acceptance of the document or
eSOMS Narrative Logs; July 2009 to June 2010
any part of it, unless this is stated in the body of the inspection report.
List of CRs for all MSPI monitored systems; July 2009 to June 2010 MSPI Derivation Reports for all MSPI monitored systems; June 2010  
1R01 Adverse Weather
CR 10-80444; Security Project - North-Side Concrete T Wall Installation Issues
4OA2 Identification and Resolution of Problems
Drawing 743-0013-00000; Topography and Storm Drain Composite; Revision D
 
EER 600631290; Perform Evaluation to Determine Locations of Drainage Gaps in Installed
CRs for the period January 1, 2010, through June 30, 2010 CR 10-81162; Potential Misapplication of TS Note; dated August 12, 2010 eSOMS Narrative Logs; July 2010, to August 2010
        T-Walls; dated August 4, 2010
eSOMS Action Tracking; July 2010 to August 2010
1R04 Equipment Alignment
WO 200322765; PDP - "New PM" Replace Rosemount STU Card; dated August 9, 2010
CR 08-42257; Annulus Exhaust Gas Treatment System (AGETS) "A" Train Low Flow
SVI-B21-T0187C, ECCS/HPCS RPV Water Level 2 and Level 8 Channel C Functional for
        Adjustment; dated June 20, 2008
1B21-N673C; Revision 6 4OA3 Follow-up of Events and Notices of Enforcement Discretion
CR 10-72614; Unplanned Fire Suppression Impairment for Annulus Exhaust Gas Treatment
  LER 2010-003; Loss of Control Rod Drive Header Pressure Result in Manual RPS Actuation;
        System; dated March 4, 2010
dated July 12, 2010 CR 10-74904; During SVI-E12T0146 Performance, Operations Received Unexpected Annunciators; dated April 4, 2010  
CR 08-34483; Annulus Exhaust Gas Treatment System Flow Indication Low Flow; dated
4OA7 Licensee-Identified Findings
        January 29, 2008
  CR 10-81724; Fuel Oil Samples not Analyzed per Tech Specs; dated August 25, 2010
CR 07-31871; AEGTS B Discharge Damper Is Not Functioning Correctly; dated
8 Attachment
        December 21, 2007
LIST OF ACRONYMS USED AEGTS  annulus exhaust gas treatment system ALARA  as-low-as-reasonably-achievable
Drawing 912-0605-00000; Reactor Building Annulus Exhaust Gas Treatment; Revision W
ASME  American Society of Mechanical Engineers
PYBP-POS-2-2; Annulus Exhaust Gas Treatment System A (B) Outage Protected Equipment
CAP  corrective action program CFR  Code of Federal Regulations CR  condition report
        Posting Checklist; Revision 10
ECC  emergency closed cooling
PNPP No. 10392; Annulus Exhaust Gas Treatment System A (B) Outage Protected Equipment
EDG  emergency diesel generator
        Posting Checklist; dated July 14, 2009
ESW  emergency service water FENOC  FirstEnergy Nuclear Operating Company HEPA  high-efficiency particulate air
SOI-M15; AEGTS System; Revision 8
HP  health physics
VLI-M23/24; MCC, Switchgear and Miscellaneous Electrical Equipment Area HVAC System;
HPCS  high pressure core spray
        Revision 7
HRA  high radiation area
CR 10-82114; 0M23C0002B Did Not Trip with a B Train Trip Signal Present; dated
IMC  Inspection Manual Chapter IP  Inspection Procedure IR  Inspection Report
        September 2, 2010
IST  inservice testing
CR 10-82118; Replacement Solenoid Valve Mount Screw Holes Are Not Threaded; dated
LCO  limiting condition for operation
        August 31, 2010
LER  Licensee Event Report LPCI  low pressure core injection MSPI  mitigating systems performance index
Drawing 912-0609-00000; MCC Switchgear and Misc Electrical Equipment Areas HVAC
NCV  non-cited violation
        System and Battery Room Exhaust; Revision AA
NEI  Nuclear Energy Institute
Perry Plant Health Report 2010-2 for P42 - Emergency Closed Cooling System
NIOSH/MSSHA National Institute for Occupational Safety and Health/  Mine Safety and Health Administration NOP  Nuclear Operating Procedure NRC  Nuclear Regulatory Commission
SOI-P42; Emergency Closed Cooling System; Revision 16
ONI  Off-Normal Instruction
VLI-P42; Emergency Closed Cooling System; Revision 15
PI  performance indicator
Drawing 302-0621-00000; Emergency Closed Cooling System; Revision SS
PM  post-maintenance RCIC  reactor core isolation cooling RHR  residual heat removal
Drawing 208-0041-00002; Reactor Protection System MG Set S001B
RP  radiation protection
Drawing 208-0041-00001; Reactor Protection System MG Set S001A
RPS  reactor protection system
CR 10-81707; Overheating on Voltage Regulator for RPS MG Set B; dated August 25, 2010
RWP  radiation work permit
                                                        2                            Attachment
SCBA  self-contained breathing apparatus SDP  Significance Determination Process SR  surveillance requirement
SSC  structure, system, or component
SVI  Surveillance Instruction 
TS  Technical Specification USAR  Updated Safety Analysis Report VHRA  very high radiation area
WO  work order 
  M. Bezilla    -2-  
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its
enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html
(the Public Electronic Reading Room).
Sincerely, 
      /RA/  Jamnes L. Cameron, Chief


Branch 6
1R05 Fire Protection (Annual/Quarterly)
Division of Reactor Projects
PAP-1910; Fire Protection Program; Revision 19
Docket No. 50-440
P54-24; Calculation of Combustible Loading and Allowable Limits for Fire Loading; Revision 4
License No. NPF-58
FPI-0IB; Pre-Fire Plan Instruction - Intermediate Building; Revision 5
FPI-0CC; Pre-Fire Plan Instruction - Control Complex; Revision 8
CR 10-80981; Documentation of NRC Questions; dated August 9, 2010
CR 10-81985; Response to Questions from the NRC Resident Inspector; dated August 27, 2010
FPI-1AB; Pre-Fire Plan Instruction - Auxiliary Building; Revision 3
CR 10-82504; NRC Question Regarding Pen Seals in AX 620 West; dated September 10, 2010
1R06 Internal Flooding
PAP-0204; Housekeeping/Cleanliness Control Program; Revision 24
ARI-H13-P601-0018; Leak Detection; Revision 13
NOP-OP-1012; Material Readiness and Housekeeping Inspection Program; Revision 5
CR 10-77685; Various Through Wall Piping Leaks on N71; dated June 3, 2010
Drawing 911-0617; Auxiliary Building Drains; Revision F
1R11 Licensed Operator Requalification Program
PYBP-PTS-0005; Operator Continuing Training Program Administration; Revision 25
PYBP-POS-0027; Operator Actions from Memory; Revision 0, dated December 3, 2008
Simulator Exercise Guide OTLC-3058201010_PY_SGC1; Cycle 10 2010 Evaluated Scenario
      C1; Revision 0
CR 10-80980; Unsat Training Observation - Ops Performance Improvement Time Not Properly
      Used; dated August 9, 2010
CR 10-81725; Unqualified Individuals Signing as Training Coordinators; dated August 25, 2010
1R12 Maintenance Effectiveness
WO 200284303; Chg Oil Fltrs Combustion Gas Purge Unit; dated July 21, 2010
CR 10-79817; Wrong Oil Added to CGMC Reservoir; dated July 17, 2010
CR 10-80089; NRC-ID. No FME High Risk Brief Sheet in Work Order; dated July 22, 2010
CR 10-80169; Failed PMT for CGMC B Aux Oil Pump; dated July 24, 2010
Clearance EPY-M25-0005; Control Room HVAC Supply Plenum; dated September 1, 2010
LCOTR# A10-M25-032; M25/26 Inoperable, Period 5 Week 10; dated August 30, 2010
CR 10-81952; Relay Contacts do not Change State; dated August 30, 2010
CR 10-81957; Loose Fittings on Low Flow Switch; dated August 30, 2010
Drawing 912-0610-00000; Control Room HVAC and Emergency Recirculation System;
      Revision FF
CR 10-82639; Maintenance HPCS Work Start Deficiencies; dated September 13, 2010
CR 10-82715; Inadequate Order for Div 3 Fuel Oil Day Tank Work; dated September 16, 2010
CR 10-82864; Grease Fitting Damaged during Disassembly; dated September 19, 2010
CR 10-82970; Less Than Adequate Contingency Planning for Div 3 DG Inspections; dated
      September 21, 2010
CR 10-82989; FME Concerns Identified in Div 3 DG Room; dated September 20, 2010
CR 10-83194; PMT Could Not Be Worked as Written; dated September 24, 2010
WO 200430281; Rebuild Ball Valves to Small and Large Seals
CR 10-83134; Lower Airlock Door Air Supply Flex Hoses Possibly Defective
CR 10-82842; Lower Airlock Pneumatic System Pressure Drop Test Failed
                                                    3                            Attachment


CR 10-76252; Lower Containment Airlock Reactor Door
Enclosure: Inspection Report 05000440/2010004  w/Attachment: Supplemental Information cc w/encl: Distribution via ListServ
CR 09-69338; Upper Containment Airlock Reactor Door
DISTRIBUTION
1R13 Maintenance Risk Assessments and Emergent Work Control
: See next page
NOP-OP-1007; Risk Management; Revision 7
CR 10-80396; Perry Not Notified of Conservative Grid Ops; dated July 28, 2010
CR 10-81724; Finding - Fuel Oil Samples not Analyzed per Tech Specs; dated August 25, 2010
CR 10-81727; Diesel Fuel Oil Sample Analysis Completion Dates Inconsistent; dated August
      25, 2010
CR 10-81733; Procedure Steps Signed as Performed Inappropriately; dated August 25, 2010
CR 10-82658; Water/Steam Leak From 1N27F505D (RFBP D Discharge Check Valve); dated
      September 15, 2010
WO 200430709; Wire Wrap/Inject Inspection Flange; dated September 17, 2010
WO 200430710; Remove Insulation @ Valve; dated September 16, 2010
ECP 10-0570-000; Leak Sealant Device on Reactor Feedwater Booster Pump D Discharge
      Check Valve (1N27F0505D); Revision 0
ECP 10-0570-001; Install and Inject Leak Sealant Device on Reactor Feedwater Booster Pump
      D Discharge Check Valve (1N27F0505D); Revision 1
CR 10-82682; Div 3 DG Generator Inter Pole Side Plate Movement; dated September 15, 2010
CR 10-82992; Div 3 Diesel Generator - Migrating Exciter Field Core Plates; dated
      September 22, 2010
WO 200430766; Remove Generator Rotor, Inspect for Loose Wedge Studs; dated
      September 15, 2010
1R15 Operability Evaluations
CR 10-78672; 1M43 Agastat Relay Qualification Issue; dated June 22, 2010
CR 10-81023; M52 Turning Vanes Degraded; dated August 10, 2010
Prompt Functionality Assessment for Degraded TSC Ventilation Supply Fan Turning Vanes;
      dated August 13, 2010
Prompt Operability Determination for Diesel Generator Building Ventilation Systems; dated
      July 15, 2010
CR 10-81973; No Insulation Inside Plenum; dated August 30, 2010
eSOMS Narrative Logs dated September 2, 2010
Prompt Operability Determination for ECC to FPCC Heat Exchanger Bypass Valve Stroke Time
  Testing Failure; August 24, 2010
CR 10-81623; OP42F0255B Failed Stroke Closed Test; dated August 23, 2010
1R18 Permanent/Temporary Modifications
Perry Plant Health Report 2010-2 for Temporary Modifications
NOP-CC-2003; Engineering Changes; Revision 14
NORM-CC-2001; Engineering Change Process Flowcharts; Revision 00
ECP 10-0020-0000; Reference Documents - Hot Surge Tank Low Level Alarm from Level
      Transmitter Signal; Revision 0
ECP 10-0020-0001; Hot Surge Tank Low Level Alarm from Level Transmitter Signal; Revision 3
WO 200399695; Hot Surge Tank Low Level Alarm; dated May 15, 2010
NOBP-ER-3003-01; Temporary Modification Review Checklist; Revision 00
CR 09-67788; Host Surge Tank (HST) Level Low Alarm Locked In; dated November 15, 2009
Drawing 302-0081-00000; Feedwater; Revision BBB
                                                  4                                Attachment


Drawing 302-0101-00000; Condensate System; Revision TT
 
Drawing 208-0149-00002; MDFP Auto Start Logic & RFBP Auto Start Logic; Revision S
CR 10-82802; Potential Single Failure Vulnerability with Hot Surge Tank Temp Mod; dated
      September 16, 2010
1R19 Post-Maintenance Testing
 
SVI-B21-T0137F; ECCS Drywell Pressure High Channel F Functional for 1B21-N694F;
      Revision 5
DOCUMENT NAME:  G:\DRPIII\Perry\PER 2010004.docm  Publicly Available
PTI-M23-P0005; Emergency Service Water Pump House Ventilation System Train B Damper
Non-Publicly Available
      Stroking; Revision 5
Sensitive  Non-Sensitive To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy
WO 200323496; Replace Rosemount MTU Card; dated August 11, 2010
  OFFICE  RIII    RIII        NAME  PVoss:dtp
WO 200323644; Replace Keylock Control Switch 1B21C-S27A; dated August 4, 2010
JCameron 
WO 200340398; Replace and Perform Calibration Check of 1M15D0001B Instrumentation;
  DATE  10/28/10 10/29/10
      dated August 25, 2010
  OFFICIAL RECORD COPY 
WO 200327715; Replace AEGT Fan B Motor; dated August 25, 2010
  Letter to M. Bezilla from J. Cameron dated October 29, 2010  
WO 200290571; Replace SLS/MTR/Oil Hydramotor at ESW B Outlet Damper; dated
      September 6, 2010
SUBJECT: PERRY NUCLEAR POWER PLANT NRC INTEGRATED INSPECTION REPORT 05000440/2010004 DISTRIBUTION
WO 200333304; MERP - Replace Utility Station w/NUS; dated September 6, 2010
: Daniel Merzke
CR 10-81632; Temperature Switch Found Tripped; dated August 23, 2010
RidsNrrPMPerry
CR 10-81633; RFACR: Damaged Field Conductor to Motor; dated August 23, 2010
WO 200328863; Replace Cntrl Relays in EH1304 Cubicle; dated September 20, 2010
SOI-R22; Metal Clad Switchgear 5-15 KV; Revision 25
CR 10-82852; Unexpected Reading Obtained during Functional Testing; dated September 19,
      2010
SVI-E22-T1319; Diesel Generator Start and Load Division 3; Revision 15
CR 10-83148; Div 3 Emergency Diesel Generator Failure to Start During Testing; dated
      September 24, 2010
CR 10-83163; Generator Stator Temperature Monitor is Erratic and Unreliable; dated
      September 24, 2010
CR 10-83181; Div 3 DG Additional Tagging Points Requested; dated September 24, 2010
1R22 Surveillance Testing
SVI-E12-T2001; RHR A Pump and Valve Operability Test; Revision 26
SVI-E12-T1194; LPCI Pump A Discharge Low Flow (Bypass) Channel Functional for 1E12-
      N652A; Revision 8
SVI-E51-T2001; RCIC Pump and Valve Operability Test; Revision 32
CR 01-79624; NRC-Identified Concern for Pre-conditioning Valve During Surveillance Testing;
      dated July 12, 2010
NOP-ER-3204; Inservice Testing Program; Revision 1
eSOMS Narrative Logs dated July 7-8, 2010
SVI-P45-T2002; ESW Pump B and Valve Operability Test; Revision 26
SVI-R10-T5227; Off-Site Power Availability Verification; Revision 2
                                                    5                            Attachment


RidsNrrDorlLpI3-2  
2RS1 Radiological Hazard Assessment and Exposure Controls
CR 09-56065; Containment Vessel Drywell Purge Degraded Flows Impacting Refuel Floor;
      dated March 25, 2009
CR 09-57294; Boundary Exceeded Radiological Controlled Area (RCA); dated April 16, 2009
CR 09-60436; Dose Rates in the P5480405 Condensate Backwash Receiving Tanl Higher than
      Expected; dated June 11, 2009
CR 09-62628; Radioactive Material Found Outside the RCA; dated August 2, 2009
CR 09-63398 and Associated Apparent Cause Evaluation; Platform Found Outside with Fixed
      Contamination; dated August 18, 2009
CR 09-66069; RISB Radioactive Material Inventory Discrepancies; dated October 16, 2009
CR 10-76774; Radiological Issues Associated with Division 2 ECC LOCA Initiation; dated
      May 11, 2010
CR-09-54403; RFO-12 Elevated Airborne Levels During Separator Lift; dated February 28, 2009
HPI-C0014; Radlock key Issue; Revision 01
HPI-H0004; Identification of Radioactive Materials and Release of Materials from RCAs;
      Revision 22
HPI-K0009; Operation of the WARF, RISB and OSSC Yard; Revision 0
HPI-L0004; Source Control Documentation and Inventory; Revision 8
NOPB-NF-3102; Control of Non-Special Nuclear Material in the Fuel Pools; Revision 00
NOP-OP-4101; Access Controls for Radiologically Controlled Areas; Revision 01
NOP-OP-4102; Radiological Postings, Labeling, and Markings; Revision 05
NOP-OP-4107; Radiation Work Permit; Revisions 4 and 5
NRC Form 748; National Source Tracking Transaction Report; dated January 12, 2009
NSTS Annual Inventory Reconciliation; dated September 9, 2009, and January 29, 2010
PNPP No. 10280; Sealed Source Leak Test Data Sheet HPI-L0004; dated January 13, 2010
PNPP No. 7445; Sealed Source Leak Test Data Sheet ORM 6.4.2; dated January 13, 2010
SVI-E31-T5190; Sealed Source Leak Test and Inventory; Revision 5
TEDE ALARA Evaluations for ALARA Plan Nos. 09-6018-02, 09-6041-00 and
10-0066; dates October 2008 and February 2010
2RS3 In-Plant Airborne Radioactivity Control and Mitigation
Air Sample Records/Collection and Evaluation Forms for Various Work Activities and Locations;
      Various Dates in March and April 2009
CR 09-57025; Air Sampling Equipment Found with Expired Calibration; dated April 09, 2009
EP-Emergency Plan for Perry Nuclear Power Plant Docket Nos. 50-440; Revision 30
HPI-G0007; Maintenance of Respiratory Protective Equipment and Operation of the Respirator
      Cleaning / Issue Facilities; Revision 21
HPI-G0008; Requalification of Respirators; Revision 07
HPI-L0003; Equipment History; Revision 06
HRI-0003; Respirator Qualification Health Assessment; Revision 02
NOP-OP-4301; Respiratory Protection Program; Revision 01
NOP-OP-4302; Issuing Respiratory Protection; Revision 00
NOP-OP-4303; Respirator Quantitative Fit Test Portacount PRO 8030; Revision 01
NOP-OP-4310; Firehawk M7 Self Contained Breathing Apparatus; Revision 04
NOP-OP-4702; Air Sampling; Revision 01
PSI-0022; Emergency Plan Training program; Revision 03
PYBP-RPS-0038; Radiologically Controlled Area HEPA Ventilation and HEPA Vacuum Unit
      Program; Revision 01
                                                    6                              Attachment


RidsNrrDirsIrib Resource
2RS4 Occupational Dose Assessment
ALARA Plan 09-6040; Suppression Pool Cleaning and Inspection; Revision 03
NOP-OP-4204; Special External Exposure Monitoring; Revision 03
NOP-OP-4204-04; Effective Dose Equivalent Dose Determination; Revision 01
NOP-OP-4205; Dose Assessment; Revision 03
NOP-OP-4206; Bioassay Program; Revision 00
NOP-OP-4503; Personnel Contamination Monitoring; Revision 02
Radiological Engineering Assessment; Source term Determination for Cycle 12 Operations;
        Undated
RWP 09-6040; RFO-12 Suppression Pool Diving Activities; Revision 03
4OA1 Performance Indicator Verification
NOBP-LP-4012; NRC Performance Indicators; Revision 3
NOBP-LP-4012-06; MSPI Data Sheets for Heat Removal System from July 2009 to June 2010;
        Revision 2
NOBP-LP-4012-07; MSPI Data Sheets for Residual Heat Removal System from July 2009 to
        June 2010; Revision 2
NOBP-LP-4012-19; MSPI Data Sheets for Emergency Service Water from July 2009 to
        June 2010; Revision 2
Mitigating Systems Performance Index Basis Document; Revision 4
PYBP-DES-0011; Mitigating Systems Performance Index; Revision 1
eSOMS Narrative Logs; July 2009 to June 2010
List of CRs for all MSPI monitored systems; July 2009 to June 2010
MSPI Derivation Reports for all MSPI monitored systems; June 2010
4OA2 Identification and Resolution of Problems
CRs for the period January 1, 2010, through June 30, 2010
CR 10-81162; Potential Misapplication of TS Note; dated August 12, 2010
eSOMS Narrative Logs; July 2010, to August 2010
eSOMS Action Tracking; July 2010 to August 2010
WO 200322765; PDP - New PM Replace Rosemount STU Card; dated August 9, 2010
SVI-B21-T0187C, ECCS/HPCS RPV Water Level 2 and Level 8 Channel C Functional for
        1B21-N673C; Revision 6
4OA3 Follow-up of Events and Notices of Enforcement Discretion
LER 2010-003; Loss of Control Rod Drive Header Pressure Result in Manual RPS Actuation;
        dated July 12, 2010
CR 10-74904; During SVI-E12T0146 Performance, Operations Received Unexpected
        Annunciators; dated April 4, 2010
4OA7 Licensee-Identified Findings
CR 10-81724; Fuel Oil Samples not Analyzed per Tech Specs; dated August 25, 2010
                                                  7                            Attachment


Steven West Steven Orth Jared Heck
                        LIST OF ACRONYMS USED
AEGTS      annulus exhaust gas treatment system
ALARA      as-low-as-reasonably-achievable
ASME        American Society of Mechanical Engineers
CAP        corrective action program
CFR        Code of Federal Regulations
CR          condition report
ECC        emergency closed cooling
EDG        emergency diesel generator
ESW        emergency service water
FENOC      FirstEnergy Nuclear Operating Company
HEPA        high-efficiency particulate air
HP          health physics
HPCS        high pressure core spray
HRA        high radiation area
IMC        Inspection Manual Chapter
IP          Inspection Procedure
IR          Inspection Report
IST        inservice testing
LCO        limiting condition for operation
LER        Licensee Event Report
LPCI        low pressure core injection
MSPI        mitigating systems performance index
NCV        non-cited violation
NEI        Nuclear Energy Institute
NIOSH/MSSHA National Institute for Occupational Safety and Health/
            Mine Safety and Health Administration
NOP        Nuclear Operating Procedure
NRC        Nuclear Regulatory Commission
ONI        Off-Normal Instruction
PI          performance indicator
PM          post-maintenance
RCIC        reactor core isolation cooling
RHR        residual heat removal
RP          radiation protection
RPS        reactor protection system
RWP        radiation work permit
SCBA        self-contained breathing apparatus
SDP        Significance Determination Process
SR          surveillance requirement
SSC        structure, system, or component
SVI        Surveillance Instruction
TS          Technical Specification
USAR        Updated Safety Analysis Report
VHRA        very high radiation area
WO          work order
                                            8                      Attachment


Allan Barker
M. Bezilla                                                                -2-
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its
enclosure will be available electronically for public inspection in the NRC Public Document
Room or from the Publicly Available Records (PARS) component of NRC's document system
(ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html
(the Public Electronic Reading Room).
                                                                          Sincerely,
                                                                          /RA/
                                                                          Jamnes L. Cameron, Chief
                                                                          Branch 6
                                                                          Division of Reactor Projects
Docket No. 50-440
License No. NPF-58
Enclosure:                Inspection Report 05000440/2010004
                            w/Attachment: Supplemental Information
cc w/encl:                Distribution via ListServ
DISTRIBUTION:
See next page
DOCUMENT NAME: G:\DRPIII\Perry\PER 2010004.docm
    Publicly Available                          Non-Publicly Available                    Sensitive                Non-Sensitive
To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy
OFFICE              RIII                                RIII
NAME                PVoss:dtp                          JCameron
DATE                10/28/10                            10/29/10
                                                          OFFICIAL RECORD COPY


Carole Ariano  
Letter to M. Bezilla from J. Cameron dated October 29, 2010
Linda Linn  
SUBJECT:      PERRY NUCLEAR POWER PLANT NRC INTEGRATED
DRPIII DRSIII Patricia Buckley  
              INSPECTION REPORT 05000440/2010004
Tammy Tomczak  
DISTRIBUTION:
Daniel Merzke
RidsNrrPMPerry
RidsNrrDorlLpI3-2
RidsNrrDirsIrib Resource
Steven West
Steven Orth
Jared Heck
Allan Barker
Carole Ariano
Linda Linn
DRPIII
DRSIII
Patricia Buckley
Tammy Tomczak
ROPreports Resource
ROPreports Resource
}}
}}

Revision as of 06:58, 13 November 2019

IR 05000440-10-004, on 07/01/2010 - 09/30/2010; Surveillance Testing; Problem Identification and Resolution
ML103020254
Person / Time
Site: Perry FirstEnergy icon.png
Issue date: 10/29/2010
From: Jamnes Cameron
NRC/RGN-III/DRP/B6
To: Bezilla M
FirstEnergy Nuclear Operating Co
References
IR-10-004
Download: ML103020254 (42)


See also: IR 05000440/2010004

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION III

2443 WARRENVILLE ROAD, SUITE 210

LISLE, IL 60532-4352

October 29, 2010

Mr. Mark Bezilla

Site Vice President

FirstEnergy Nuclear Operating Company

Perry Nuclear Power Plant

P. O. Box 97, 10 Center Road, A-PY-A290

Perry, OH 44081-0097

SUBJECT: PERRY NUCLEAR POWER PLANT NRC INTEGRATED

INSPECTION REPORT 05000440/2010004

Dear Mr. Bezilla:

On September 30, 2010, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at your Perry Nuclear Power Plant. The enclosed report documents the inspection

findings which were discussed on October 6, 2010, with you and members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Based on the results of this inspection, two NRC-identified findings of very low safety

significance (Green) were identified. Both of the findings were determined to involve a violation

of NRC requirements, however, because the findings were of very low safety significance and

because the issues were entered into your corrective action program, the NRC is treating the

findings as non-cited violations (NCVs) consistent with Section 2.3.2 of the NRC Enforcement

Policy.

If you contest the subject or severity of these NCVs, you should provide a response

within 30 days of the date of this inspection report, with the basis for your denial, to the

U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington,

DC 20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory

Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the

Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC

20555-0001; and the Resident Inspector Office at the Perry Nuclear Power Plant.

In addition, if you disagree with the cross-cutting aspect of any finding in this report, you

should provide a response within 30 days of the date of this inspection report, with the basis

for your disagreement, to the Regional Administrator, Region III, and the NRC Resident

Inspector at the Perry Nuclear Power Plant.

M. Bezilla -2-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its

enclosure will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records (PARS) component of NRC's document system

(ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html

(the Public Electronic Reading Room).

Sincerely,

/RA/

Jamnes L. Cameron, Chief

Branch 6

Division of Reactor Projects

Docket No. 50-440

License No. NPF-58

Enclosure: Inspection Report 05000440/2010004

w/Attachment: Supplemental Information

cc w/encl: Distribution via ListServ

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket No: 50-440

License No: NPF-58

Report No: 050000440/2010004

Licensee: FirstEnergy Nuclear Operating Company (FENOC)

Facility: Perry Nuclear Power Plant, Unit 1

Location: Perry, Ohio

Dates: July 1, 2010, through September 30, 2010

Inspectors: M. Marshfield, Senior Resident Inspector

T. Hartman, Resident Inspector

R. Edwards, Reactor Inspector

L. Jones, Reactor Engineer

M. Phalen, Senior Health Physicist, DRS

W. Slawinski, Senior Health Physicist, DRS

P. Smagacz, Reactor Engineer

Observers: V. Myers, Nuclear Safety Professional Development

Program

R. Leidy, Ohio Department of Health

Approved by: Jamnes L. Cameron, Chief

Branch 6

Division of Reactor Projects

Enclosure

TABLE OF CONTENTS

SUMMARY OF FINDINGS ........................................................................................................... 1

REPORT DETAILS ....................................................................................................................... 3

Summary of Plant Status ........................................................................................................... 3

1. REACTOR SAFETY ....................................................................................................... 3

1R01 Adverse Weather Protection (71111.01) ............................................................. 3

1R04 Equipment Alignment (71111.04Q) ..................................................................... 3

1R05 Fire Protection (71111.05Q)................................................................................ 5

1R06 Flood Protection Measures (71111.06) ............................................................... 5

1R11 Licensed Operator Requalification Program (71111.11) ..................................... 6

1R12 Maintenance Effectiveness (71111.12Q) ............................................................ 6

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13) ......... 7

1R15 Operability Evaluations (71111.15) ..................................................................... 8

1R18 Temporary Plant Modifications (71111.18) ......................................................... 9

1R19 Post-Maintenance Testing (71111.19) ................................................................ 9

1R22 Surveillance Testing (71111.22) ....................................................................... 10

2. RADIATION SAFETY ................................................................................................... 13

2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01) ............. 13

2RS3 In-Plant Airborne Radioactivity Control and Mitigation (71124.03) ................... 17

2RS4 Occupational Dose Assessment (71124.04) ..................................................... 20

4. OTHER ACTIVITIES ..................................................................................................... 21

4OA1 Performance Indicator Verification (71151)....................................................... 21

4OA2 Problem Identification and Resolution (71152) ................................................. 23

4OA3 Follow-up of Events and Notices of Enforcement Discretion (71153) ............... 26

4OA5 Other Activities .................................................................................................. 27

4OA6 Meetings............................................................................................................ 28

4OA7 Licensee-Identified Violations ........................................................................... 28

SUPPLEMENTAL INFORMATION ............................................................................................... 1

Key Points of Contact ................................................................................................................ 1

List of Items Opened, Closed and Discussed............................................................................ 1

List of Documents Reviewed ..................................................................................................... 2

List of Acronyms Used .............................................................................................................. 8

Enclosure

SUMMARY OF FINDINGS

IR 05000440/2010004; 07/01/2010 - 09/30/2010; Surveillance Testing; Problem Identification

and Resolution.

The inspection was conducted by resident and regional inspectors. The inspection report

(IR) covers a 3-month period of resident inspection. Two green findings which were NCVs were

identified. The significance of most findings is indicated by their color (Green, White, Yellow, or

Red) using Inspection Manual Chapter (IMC) 0609 Significance Determination Process (SDP).

Cross-cutting aspects were determined using IMC 0310, "Components Within The Cross-

Cutting Areas." Findings for which the SDP does not apply may be "Green," or be assigned a

severity level after NRC management review. The NRC's program for overseeing the safe

operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor

Oversight Process," Revision 4, dated December 2006.

A. Inspector-Identified and Self-Revealed Findings

Cornerstone: Mitigating Systems

  • Green. The inspectors identified a finding of very low safety significance and associated

NCV of 10 CFR 50, Appendix B, Criterion XI, Test Control, for the unacceptable

preconditioning of the 'A' residual heat removal (RHR) pump minimum flow valve prior to

quarterly in-service testing. Specifically, the licensee performed a surveillance that

cycled the valve prior to performing stroke time testing, and had not previously

performed an evaluation assessing the sequence for preconditioning. The licensee

entered the issue into their corrective action program.

The inspectors determined that unacceptably preconditioning the RHR minimum flow

valve was a performance deficiency that affected the Mitigating Systems Cornerstone

because it can mask the true as-found condition of a component designed to mitigate

accidents. The performance deficiency was determined to be more than minor because,

if left uncorrected, it could lead to a more significant safety concern. The finding was of

very low safety significance because it was not a design/qualification deficiency, did not

represent a loss of system safety function, did not result in a loss of function of a single

train for greater than its Technical Specification (TS)-allowable outage time, did not

result in a loss of function of nonsafety-related risk-significant equipment and was not

risk significant due to external events. This finding has a cross-cutting aspect in the

work control planning component of the Human Performance area (per

IMC 0310 H.3(a)), because the licensee did not appropriately plan work activities for

plant structures, systems, and components. Specifically, the licensee did not schedule

the surveillance tests in the proper sequence to prevent unacceptable preconditioning of

the valve. (Section 1R22)

  • Green. The inspectors identified a finding of very low safety significance and associated

NCV for a failure to comply with TS 3.0.2 by not entering TS Limiting Condition for

Operation (LCO) 3.3.5.1 Condition A and TS LCO 3.3.6.1 Condition A when required.

The inspectors determined that the licensee incorrectly utilized a TS Surveillance

Requirement Note that allows a delay in entering the Conditions and Required Actions

for the given TS LCO. As a result, the licensee failed to correctly enter the Conditions

and Required Actions when reactor level instruments were declared inoperable to

1 Enclosure

perform testing in support of planned maintenance. The licensee entered the issue

associated with the failure to comply with TS into their corrective action program.

This performance deficiency was determined to be more than minor because it impacted

the Equipment Performance attribute of the Mitigating Systems Cornerstone, and

adversely affected the cornerstone objective to ensure the availability, reliability, and

capability of systems that respond to initiating events to prevent undesirable

consequences (i.e., core damage); and if left uncorrected it could lead to a more

significant safety concern. This finding is of very low safety significance because it was

not a design/qualification deficiency, did not represent a loss of system safety function,

did not result in a loss of function of a single train for greater than its TS-allowable

outage time, did not result in a loss of function of nonsafety-related risk-significant

equipment and was not risk significant due to external events. This finding has a

cross-cutting aspect in the decision making component of Human Performance

cross-cutting area (per IMC 0310 H.1(a)), because the licensee did not use conservative

assumptions to ensure the proposed action was safe. Specifically, the licensee

incorrectly used the TS Surveillance Requirement Note to satisfy maintenance

requirements. (Section 4OA2)

B. Licensee-Identified Violations

One violation of very low safety significance was identified by the licensee and

has been reviewed by the inspectors. Corrective actions taken or planned by the

licensee have been entered into the licensee's corrective action program. This

violation and its corrective action tracking number are listed in Section 4OA7 of

this report.

2 Enclosure

REPORT DETAILS

Summary of Plant Status

The plant began the inspection period at 100 percent power. With the exception of minor

reductions in power to support routine surveillances and rod pattern adjustments, and several

occasions when the plant reduced power because of plant cooling limitations caused by

summer environmental conditions, the plant remained at full power for the entire period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and

Emergency Preparedness

1R01 Adverse Weather Protection (71111.01)

External Flooding

a. Inspection Scope

The inspectors evaluated the design, material condition, and procedures for coping with

the design basis probable maximum flood. The evaluation included a review to check

for deviations from the descriptions provided in the Updated Safety Analysis Report

(USAR) for features intended to mitigate the potential for flooding from external factors.

As part of this evaluation, the inspectors checked for obstructions that could prevent

draining, checked that the roofs did not contain obvious loose items that could clog

drains in the event of heavy precipitation, and determined that barriers required to

mitigate the flood were in place and operable. Additionally, the inspectors performed a

walkdown of the protected area to identify any modification to the site which would inhibit

site drainage during a probable maximum precipitation event or allow water ingress past

a barrier. The inspectors walked down underground bunkers/manholes subject to

flooding that contained multiple train or multi-function risk-significant cables. The

inspectors also reviewed the Off-Normal Instructions (ONIs) for mitigating the design

basis flood to ensure it could be implemented as written.

This inspection constituted one sample of external flooding as defined in Inspection

Procedure (IP) 71111.01-05.

b. Findings

No findings were identified.

1R04 Equipment Alignment (71111.04Q)

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant

systems:

  • 'B' annulus exhaust gas treatment system (AEGTS) on July 7, 2010;
  • 'A' motor control center, switchgear and miscellaneous electrical equipment

heating ventilation and air conditioning system on September 2, 2010; and

3 Enclosure

RPS motor generator set was out of service on September 30, 2010.

The inspectors selected these systems based on their risk-significance relative to the

Reactor Safety Cornerstone at the time they were inspected. The inspectors attempted

to identify any discrepancies that could impact the function of the system, and, therefore,

potentially increase risk. The inspectors reviewed applicable operating procedures,

system diagrams, USAR, Technical Specification (TS) requirements, outstanding work

orders (WOs), condition reports (CRs), and the impact of ongoing work activities on

redundant trains of equipment in order to identify conditions that could have rendered

the systems incapable of performing their intended functions. The inspectors also

walked down accessible portions of the systems to verify system components and

support equipment were aligned correctly and operable. The inspectors examined the

material condition of the components and observed operating parameters of equipment

to verify that there were no obvious deficiencies. The inspectors also verified that the

licensee had properly identified and resolved equipment alignment problems that could

cause initiating events or impact the capability of mitigating systems or barriers and

entered them into the corrective action program (CAP) with the appropriate significance

characterization. Documents reviewed are listed in the Attachment.

These inspections constituted three partial system walkdown samples for equipment

alignment as defined in IP 71111.04-05.

b. Findings

No findings were identified.

.2 Semi-Annual Complete System Walkdown

a. Inspection Scope

On September 24, 2010, the inspectors concluded a complete system alignment

inspection of the emergency closed cooling (ECC) system to verify the functional

capability of the system. This system was selected because it was considered both

safety significant and risk significant in the licensees probabilistic risk assessment.

The inspectors walked down the system to review mechanical and electrical equipment

line-ups, electrical power availability, system temperature indications, component

labeling, component lubrication, component and equipment cooling, hangers and

supports, operability of support systems, and to ensure that ancillary equipment or

debris did not interfere with equipment operation. A review of a sample of past and

outstanding WOs was performed to determine whether any deficiencies significantly

affected the system function. In addition, the inspectors reviewed the CAP database to

ensure that system equipment alignment problems were being identified and

appropriately resolved. Documents reviewed are listed in the Attachment.

This inspection constituted one complete system walkdown sample as defined in

IP 71111.04-05.

b. Findings

No findings were identified.

4 Enclosure

1R05 Fire Protection (71111.05Q)

a. Inspection Scope

The inspectors conducted fire protection walkdowns which were focused on availability,

accessibility, and the condition of firefighting equipment in the following risk-significant

plant areas:

  • Fire Zone 0IB-4; Intermediate Building 654'-6" Elevation;
  • Fire Zone 0IB-3; Intermediate Bldg 620' Elevation;
  • Fire Zone 0CC-2; Control Complex 599' Elevation;
  • Fire Zone 0IB-1; Intermediate Bldg 574' Elevation; and
  • Fire Zone 1AB-3B; Auxiliary Building 620'-6" Elevation West.

The inspectors reviewed areas to assess if the licensee had implemented a fire

protection program that adequately controlled combustibles and ignition sources within

the plant, effectively maintained fire detection and suppression capability, maintained

passive fire protection features in good material condition, and implemented adequate

compensatory measures for out-of-service, degraded, or inoperable fire protection

equipment, systems, or features in accordance with the licensees fire plan. The

inspectors selected fire areas based on their overall contribution to internal fire risk as

documented in the plants Individual Plant Examination of External Events with later

additional insights, their potential to impact equipment which could initiate or mitigate a

plant transient, or their impact on the plants ability to respond to a security event. Using

the documents listed in the Attachment, the inspectors verified that fire hoses and

extinguishers were in their designated locations and available for immediate use; that

fire detectors and sprinklers were unobstructed; that transient material loading was

within the analyzed limits; and fire doors, dampers, and penetration seals appeared to

be in satisfactory condition. The inspectors also verified that minor issues identified

during the inspection were entered into the licensees CAP. Documents reviewed are

listed in the Attachment to this report.

These activities constituted five quarterly fire protection inspection samples as defined in

IP 71111.05-05.

b. Findings

No findings were identified.

1R06 Flood Protection Measures (71111.06)

a. Inspection Scope

The inspectors reviewed selected risk important plant design features and licensee

procedures intended to protect the plant and its safety-related equipment from internal

flooding events. The inspectors reviewed flood analyses and design documents,

including the USAR, engineering calculations, and ONI's to identify licensee

commitments. The specific documents reviewed are listed in the Attachment to this

report. In addition, the inspectors reviewed licensee drawings to identify areas and

equipment that may be affected by internal flooding caused by the failure or

misalignment of nearby sources of water, such as the fire suppression or the circulating

5 Enclosure

water systems. The inspectors also reviewed the licensees corrective action documents

with respect to past flood-related items identified in the CAP to verify the adequacy of

the corrective actions.

The inspectors performed a walkdown of the low pressure core spray areas to assess

the adequacy of watertight doors and verify drains and sumps were clear of debris and

were operable, and that the licensee complied with its commitments.

This inspection constituted one internal flooding sample as defined in IP 71111.06-05.

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification Program (71111.11)

a. Inspection Scope

On August 30, 2010, the inspectors observed a crew of licensed operators in the plants

simulator during licensed operator requalification examinations to verify that operator

performance was adequate, evaluators were identifying and documenting crew

performance problems, and training was being conducted in accordance with licensee

procedures. The inspectors evaluated the following areas:

  • licensed operator performance;
  • crews clarity and formality of communications;
  • ability to take timely actions in the conservative direction;
  • prioritization, interpretation, and verification of annunciator alarms;
  • correct use and implementation of abnormal and emergency procedures;
  • control board manipulations;
  • oversight and direction from supervisors; and
  • the ability to identify and implement appropriate TS actions and Emergency Plan

actions and notifications.

The crews performance in these areas was compared to pre-established operator action

expectations and successful critical task completion requirements. Documents reviewed

are listed in the Attachment to this report.

This inspection constituted one quarterly operator license requalification program sample

as defined in IP 71111.11.

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness (71111.12Q)

a. Inspection Scope

The inspectors evaluated degraded performance issues involving the following

risk-significant systems:

6 Enclosure

  • 'B' compressible gas mixing compressor;
  • 'A' control room ventilation system;

(HPCS) system; and

  • Upper and lower containment airlocks.

The inspectors reviewed events such as where ineffective equipment maintenance had

resulted in valid or invalid automatic actuations of engineered safeguards systems and

independently verified the licensee's actions to address system performance or condition

problems in terms of the following:

  • implementing appropriate work practices;
  • identifying and addressing common cause failures;
  • scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;
  • characterizing system reliability issues for performance;
  • charging unavailability for performance;
  • trending key parameters for condition monitoring;
  • verifying appropriate performance criteria for structures, systems, and

components/functions classified as (a)(2), or appropriate and adequate goals and

corrective actions for systems classified as (a)(1).

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. In addition, the inspectors verified maintenance

effectiveness issues were entered into the CAP with the appropriate significance

characterization. Documents reviewed are listed in the Attachment to this report.

This inspection constituted four quarterly maintenance effectiveness samples as defined

in IP 71111.12-05.

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

a. Inspection Scope

The inspectors reviewed the licensee's evaluation and management of plant risk for the

maintenance and emergent work activities affecting risk-significant and safety-related

equipment listed below to verify that the appropriate risk assessments were performed

prior to removing equipment for work:

  • conservative grid operations on July 15, 2010;
  • work on control rod drive pump 'B' concurrent with testing of the Division 3 EDG

on August 17, 2010;

  • EDG fuel oil samples on August 26, 2010;
  • reactor feed booster pump discharge check valve repair during the week of

September 13, 2010; and

  • HPCS diesel generator repairs during the week of September 15, 2010.

7 Enclosure

These activities were selected based on their potential risk significance relative to the

Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that

risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate

and complete. When emergent work was performed, the inspectors verified that the

plant risk was promptly reassessed and managed. The inspectors reviewed the scope

of maintenance work, discussed the results of the assessment with the licensee's

probabilistic risk analyst or shift technical advisor, and verified plant conditions were

consistent with the risk assessment. The inspectors also reviewed TS requirements and

walked down portions of redundant safety systems, when applicable, to verify risk

analysis assumptions were valid and applicable requirements were met.

These maintenance risk assessments and emergent work control activities constituted

five samples as defined in IP 71111.13-05.

b. Findings

No findings were identified.

1R15 Operability Evaluations (71111.15)

a. Inspection Scope

The inspectors reviewed the following issues:

  • EDG ventilation systems with installed relays beyond the 20-year qualification

life;

failed stroke time testing; and

  • 'A' control room ventilation plenum missing insulation.

The inspectors selected these potential operability issues based on the risk-significance

of the associated components and systems. The inspectors evaluated the technical

adequacy of the evaluations to ensure that TS operability was properly justified and the

subject component or system remained available such that no unrecognized increase in

risk occurred. The inspectors compared the operability and design criteria in the

appropriate sections of the TS and USAR to the licensees evaluations to determine

whether the components or systems were operable. Where compensatory measures

were required to maintain operability, the inspectors determined whether the measures

in place would function as intended and were properly controlled. The inspectors

determined, where appropriate, compliance with bounding limitations associated with the

evaluations. Additionally, the inspectors reviewed a sampling of corrective action

documents to verify that the licensee was identifying and correcting any deficiencies

associated with operability evaluations. Documents reviewed are listed in the

Attachment to this report.

This operability inspection constituted four samples as defined in IP 71111.15-05.

b. Findings

No findings were identified.

8 Enclosure

1R18 Temporary Plant Modifications (71111.18)

a. Inspection Scope

The inspectors reviewed the temporary modification for the Hot Surge Tank Hi/Low

Level Alarm. The inspectors compared the temporary configuration changes and

associated 10 CFR 50.59 screening and evaluation information against the design basis,

the USAR, and the TS, as applicable, to verify that the modification did not affect the

operability or availability of the affected system(s). The inspectors also compared the

licensees information to operating experience information to ensure that lessons learned

from other utilities had been incorporated into the licensees decision to implement the

temporary modification. The inspectors, as applicable, performed field verifications to

ensure that the modifications were installed as directed; the modifications operated as

expected; modification testing adequately demonstrated continued system operability,

availability, and reliability; and that operation of the modifications did not impact the

operability of any interfacing systems. Lastly, the inspectors discussed the temporary

modification with operations, engineering, and training personnel to ensure that the

individuals were aware of how extended operation with the temporary modification in

place could impact overall plant performance. Documents reviewed in the course of this

inspection are listed in the Attachment to this report.

This inspection constituted one sample of a temporary modification as defined in

IP 71111.18-05.

b. Findings

No findings were identified.

1R19 Post-Maintenance Testing (71111.19)

a. Inspection Scope

The inspectors reviewed the following post-maintenance (PM) activities to verify that

procedures and test activities were adequate to ensure system operability and functional

capability:

  • high drywell pressure master trip unit replacement during the week of

August 9, 2010;

  • AEGTS fan replacement during the week of August 25, 2010;

work during the week of September 7, 2010;

  • HPCS pump breaker relay replacement during the week of September 17, 2010;

and

  • Division 3 EDG outage retest during the week of September 24, 2010.

These activities were selected based upon the structure, system, or component's ability

to impact risk. The inspectors evaluated these activities for the following (as applicable):

  • the effect of testing on the plant had been adequately addressed;
  • testing was adequate for the maintenance performed;

9 Enclosure

  • acceptance criteria were clear and demonstrated operational readiness;
  • test instrumentation was appropriate;
  • tests were performed as written in accordance with properly reviewed and

approved procedures;

  • equipment was returned to its operational status following testing (temporary

modifications or jumpers required for test performance were properly removed

after test completion); and

  • test documentation was properly evaluated.

The inspectors evaluated the activities against TS, the USAR, 10 CFR Part 50

requirements, licensee procedures, and various NRC generic communications to ensure

that the test results adequately ensured that the equipment met the licensing basis and

design requirements. In addition, the inspectors reviewed corrective action documents

associated with PM tests to determine whether the licensee was identifying problems

and entering them in the CAP and that the problems were being corrected

commensurate with their importance to safety. Documents reviewed are listed in the

Attachment to this report.

This inspection constituted six PM testing samples as defined in IP 71111.19-05.

b. Findings

No findings were identified.

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors reviewed the test results for the following activities to determine whether

risk-significant systems and equipment were capable of performing their intended safety

function and to verify testing was conducted in accordance with applicable procedural

and TS requirements:

week of July 12, 2010 (IST);

week of July 23, 2010 (routine);

week of August 2, 2010 (routine); and

  • ESW 'B' pump and valve operability testing during the week of August 13, 2010

(routine).

The inspectors observed in-plant activities and reviewed procedures and associated

records to determine the following:

  • did preconditioning occur;
  • were the effects of the testing adequately addressed by control room personnel

or engineers prior to the commencement of the testing;

  • were acceptance criteria clearly stated, demonstrated operational readiness, and

consistent with the system design basis;

  • plant equipment calibration was correct, accurate, and properly documented;

10 Enclosure

  • as-left setpoints were within required ranges, and the calibration frequency were

in accordance with TS, the USAR, procedures, and applicable commitments;

  • measuring and test equipment calibration was current;
  • test equipment was used within the required range and accuracy;
  • applicable prerequisites described in the test procedures were satisfied;
  • test frequencies met TS requirements to demonstrate operability and reliability;
  • tests were performed in accordance with the test procedures and other

applicable procedures;

  • jumpers and lifted leads were controlled and restored where used;
  • test data and results were accurate, complete, within limits, and valid;
  • test equipment was removed after testing;
  • where applicable for IST activities, testing was performed in accordance with the

applicable version of Section XI, American Society of Mechanical Engineers

(ASME) Code, and reference values were consistent with the system design

basis;

  • where applicable, test results not meeting acceptance criteria were addressed

with an adequate operability evaluation or the system or component was

declared inoperable;

  • where applicable for safety-related instrument control surveillance tests,

reference setting data were accurately incorporated in the test procedure;

  • where applicable, actual conditions encountering high resistance electrical

contacts were such that the intended safety function could still be accomplished;

  • prior procedure changes had not provided an opportunity to identify problems

encountered during the performance of the surveillance or calibration test;

  • equipment was returned to a position or status required to support the

performance of its safety functions; and

  • all problems identified during the testing were appropriately documented and

dispositioned in the CAP.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted three routine surveillance testing samples and one inservice

testing sample as defined in IP 71111.22, Sections -02 and -05.

b. Findings

Introduction: The inspectors identified a finding of very low safety significance (Green)

and associated NCV of 10 CFR Part 50, Appendix B, Criterion XI, Test Control, for

unacceptable preconditioning of the 'A' RHR pump minimum flow valve prior to quarterly

IST. Specifically, the surveillance test sequencing caused this valve to be opened and

closed before the documented stroke time testing, and the sequence had not been

evaluated for preconditioning prior to performance of the tests.

Description: On July 8, 2010, at approximately 9:30 a.m., the inspectors observed the

performance of surveillance test SVI-E12-T2001, RHR A Pump and Valve Operability

Test. Included in this test is the quarterly timed valve stroke of 1E12-F0064A, RHR

Pump A Min Flow Valve, as required by the IST program. During review of the previous

shift narrative logs, it was identified that surveillance test SVI-E12-T1194, LPCI (Low

Pressure Core Injection) Pump A Discharge Low Flow (Bypass) Channel Functional for

1E12-N652A, was performed at around 1:30 a.m. This surveillance calibrates

11 Enclosure

instrument 1E12-N652A, LPCI Pump A Discharge Low Flow Instrument. The calibration

of the low flow instrument results in the 'A' train RHR pump minimum flow valve stroking.

This sequence of testing fully cycled the valve several times less than 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> prior to

obtaining the IST stroke timing data during SVI-E12-T2001.

Inspection Manual Technical Guidance 9900 defines unacceptable preconditioning, in

part, as The alteration; variation; manipulation; or adjustment of the physical condition

of a structure, system, and component (SSC) before or during TS surveillance or ASME

Code testing that will alter one or more of an SSCs operational parameters, which

results in acceptable test results. Such changes could mask the actual as-found

condition of the SSC and possibly result in an inability to verify the operability of the

SSC. In addition, unacceptable preconditioning could make it difficult to determine

whether the SSC would perform its intended function during an event in which the SSC

might be needed. Technical Guidance 9900 further describes that some types of

preconditioning may be considered acceptable, but that this preconditioning should

have been evaluated and documented in advance of the surveillance. Since the

licensee had not performed an evaluation which justified that preconditioning of the valve

was acceptable prior to completing the testing, the licensees surveillance testing

sequence that cycled the valve prior to obtaining stroke time data constituted

unacceptable preconditioning of the valve.

Additionally, the unacceptable preconditioning of the RHR valve was not in accordance

with the licensees procedural guidance regarding IST. Licensee Nuclear Operating

Procedure (NOP)-ER-3204, Inservice Testing Program, states, in part, Maintenance

activities should not be scheduled to influence the results of upcoming tests. Such

actions, known as preconditioning, should be avoided. In addition it also states, in part,

Care should be taken to ensure that procedures, surveillances, or tasks are not

scheduled such that unacceptable preconditioning of a component prior to the inservice

test occurs. Where unacceptable preconditioning would occur, the procedure/task

should specify that an as found test be performed first.

The licensee performed an investigation which revealed that, historically, these two

surveillances had been completed in either sequence without significant differences in

measured stroke time. As a result, the licensee determined that the preconditioning did

not significantly affect the IST stroke timing of the valve. The licensee used this

information to support an operability declaration for the system.

Analysis: The inspectors determined that stroking of the RHR minimum flow valve prior

to as-found stroke timing constituted unacceptable preconditioning and a performance

deficiency. Specifically, performing the IST surveillance test in this sequence may not

accurately indicate potential valve degradation. The inspectors determined that the

performance deficiency affected the Mitigating Systems Cornerstone, because it could

mask the true as-found condition of a component designed to mitigate accidents. The

inspectors evaluated the performance deficiency in accordance with Inspection Manual

Change (IMC) 0612, Appendix B, Issue Screening. This performance deficiency was

compared to, and was not similar to any of, the examples in IMC 0612, Appendix E,

Examples of Minor Issues, but was characterized as more than minor because, if left

uncorrected, it could lead to a more significant safety concern.

The inspectors determined the finding could be evaluated using the SDP in

accordance with IMC 0609, Significance Determination Process, Attachment 0609.04,

12 Enclosure

Phase 1 - Initial Screening and Characterization of Findings, Table 3b for the Mitigating

Systems Cornerstone. The inspectors determined the finding was of very low risk

significance because it was not a design/qualification deficiency, did not represent a loss

of system safety function, did not result in a loss of function of a single train for greater

than its TS allowable outage time, did not result in a loss of function of nonsafety-related

risk-significant equipment, and was not risk significant due to external events.

This finding has a cross-cutting aspect in the work control planning component of the

Human Performance cross-cutting area (per IMC 0310 H.3(a)), because the licensee did

not appropriately plan work activities for plant SSCs and components. Specifically, the

licensee did not schedule the surveillance tests in the proper sequence to prevent

unacceptable preconditioning of the valve.

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion XI, Test Control, states, in

part, that A test program shall be established to assure that all testing required to

demonstrate that structures, systems, and components will perform satisfactorily in

service is identified and performed in accordance with written test procedures which

incorporate the requirements and acceptance limits contained in applicable design

documents. Contrary to this requirement, on July 8, 2010, the licensee stroked

1E12-F0064A, RHR Pump A Min Flow Valve for test procedure SVI-E12-T1194 prior to

performing IST stroke timing, and failed to prevent unacceptable pre-conditioning of the

pump minimum flow valve. Because this finding is of very low safety significance and

because it was entered into the licensees CAP as CR 10-79624, this violation is being

treated as an Non-Cited Violation (NCV) consistent with Section 2.3.2 of the NRC

Enforcement Policy. (NCV 05000440/2010004-01; Unacceptable Preconditioning of

RHR Valve Prior to ASME In-Service Testing.)

2. RADIATION SAFETY

Cornerstones: Public and Occupational Radiation Safety

2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01)

The inspection activities supplement those documented in Inspection Report (IR) 05000440/2010003, and constitute one complete sample as defined in

IP 71124.01-05.

.1 Radiological Hazard Assessment (02.02)

a. Inspection Scope

The inspectors determined if there had been changes to plant operations since the last

inspection that could result in a significant new radiological hazard for onsite workers or

members of the public. The inspectors evaluated whether the licensee assessed the

potential impact of these changes and has implemented periodic monitoring, as

appropriate, to detect and quantify the radiological hazard.

The inspectors reviewed the last two radiological surveys from selected plant areas.

The inspectors evaluated whether the thoroughness and frequency of the surveys were

appropriate for the given radiological hazards.

13 Enclosure

The inspectors conducted walkdowns of the facility, including radioactive waste

processing, storage, and handling areas to evaluate material conditions and performed

independent radiation measurements to verify conditions.

The inspectors observed work in potential airborne areas and evaluated whether the air

samples were representative of the breathing air zone. The inspectors evaluated

whether continuous air monitors were located in areas with low background to minimize

false alarms and representative of actual work areas. The inspectors evaluated the

licensees program for monitoring levels of loose surface contamination in areas of the

plant with the potential for the contamination to become airborne.

b. Findings

No findings were identified.

.2 Instructions to Workers (02.03)

a. Inspection Scope

The inspectors selected various containers holding nonexempt licensed radioactive

materials that may cause unplanned or inadvertent exposure of workers, and assessed

whether the containers were labeled and controlled in accordance with 10 CFR 20.1904,

Labeling Containers, or met the requirements of 10 CFR 20.1905(g).

For work activities that could suddenly and severely increase radiological conditions, the

inspectors assessed the licensees means to inform workers of changes that could

significantly impact their occupational dose.

b. Findings

No findings were identified.

.3 Contamination and Radioactive Material Control (02.04)

a. Inspection Scope

The inspectors observed several locations where the licensee monitors potentially

contaminated material leaving the radiologically controlled area and evaluated the

methods used for the control, survey, and release of materials from these areas. The

inspectors also observed the performance of personnel surveying and releasing material

for unrestricted use to determine if the methods used were in accordance with

procedures and whether those procedures were sufficient to control the spread of

contamination and prevent unintended release of materials from the site. The inspectors

determined whether radiation monitoring instrumentation used for these surveys had

appropriate sensitivity for the types of radiation present.

The inspectors reviewed the licensees criteria for the survey and release of potentially

contaminated material to determine if there was guidance on how to respond to an alarm

that indicates the presence of licensed radioactive material.

The inspectors reviewed the licensees procedures and records to verify that the

radiation detection instrumentation was used at its typical sensitivity level based on

14 Enclosure

appropriate counting parameters. The inspectors assessed whether or not the licensee

established a de facto release limit by altering the instruments typical sensitivity

through such methods as raising the energy discriminator level or locating the instrument

in a high-radiation background area.

The inspectors selected three sealed sources from the licensees inventory records and

assessed whether the sources were accounted for and verified to be intact (i.e., they

were not leaking their radioactive content).

The inspectors evaluated whether any transactions, since the last inspection, involving

nationally tracked sources were reported in accordance with 10 CFR 20.2207.

b. Findings

No findings were identified.

.4 Radiological Hazards Control and Work Coverage (02.05)

a. Inspection Scope

The inspectors evaluated ambient radiological conditions (e.g., radiation levels or

potential radiation levels) during tours of the facility. The inspectors assessed whether

the conditions were consistent with applicable posted surveys, radiation work permits

(RWPs), and worker briefings. The inspectors reviewed RWPs for work within airborne

radioactivity areas with the potential for individual worker internal exposures. For these

RWPs, the inspectors evaluated airborne radioactive controls and monitoring, including

potential for significant airborne levels (e.g., grinding, grit blasting, system breaches,

entry into tanks, cubicles, and reactor cavities). The inspectors assessed barrier (e.g.,

tent or glove box) integrity and temporary high-efficiency particulate air (HEPA)

ventilation system operation for selected airborne radioactive material areas

The inspectors examined the licensees physical and programmatic controls for highly

activated or contaminated materials (nonfuel) stored within spent fuel and other storage

pools. The inspectors assessed whether appropriate controls (i.e., administrative and

physical controls) were in place to preclude inadvertent removal of these materials from

the pool.

The inspectors examined the posting and physical controls for selected high-radiation

areas (HRAs) and very-high-radiation areas (VHRAs) to verify conformance with the

occupational performance indicator (PI).

b. Findings

No findings were identified.

.5 Risk-Significant High-Radiation Area and Very High-Radiation Area Controls (02.06)

a. Inspection Scope

The inspectors discussed with the radiation protection (RP) manager the controls and

procedures for HRAs and VHRAs. The inspectors discussed methods employed by the

licensee to provide stricter control of VHRA access as specified in 10 CFR 20.1602,

15 Enclosure

Control of Access to Very High-Radiation Areas, and Regulatory Guide 8.38, Control

of Access to High and Very High-Radiation Areas of Nuclear Plants. The inspectors

assessed whether any changes to licensee procedures substantially reduced the

effectiveness and level of worker protection.

The inspectors discussed the controls in place for special areas that have the potential

to become VHRAs during certain plant operations with first-line health physics (HP)

supervisors (or equivalent positions having backshift HP oversight authority). The

inspectors assessed whether these plant operations required communication

beforehand with the HP group, so as to allow corresponding timely actions to properly

post, control, and monitor the radiation hazards including re-access authorization.

The inspectors evaluated licensee controls for VHRAs and areas with the potential to

become a VHRA to ensure that an individual was not able to gain unauthorized access

to the VHRA.

b. Findings

No findings were identified.

.6 Radiation Worker Performance (02.07)

a. Inspection Scope

The inspectors observed radiation worker performance with respect to stated RP work

requirements. The inspectors assessed whether workers were aware of the radiological

conditions in their workplace and the RWP controls/limits in place, and whether their

performance reflected the level of radiological hazards present.

The inspectors reviewed a maximum of 10 radiological problem reports since the last

inspection that found the cause of the event to be human performance errors. The

inspectors evaluated whether there was an observable pattern traceable to a similar

cause. The inspectors assessed whether this perspective matched the corrective action

approach taken by the licensee to resolve the reported problems. The inspectors

discussed with the RP manager any problems with the corrective actions planned or

taken.

b. Findings

No findings were identified.

.7 Radiation Protection Technician Proficiency (02.08)

a. Inspection Scope

The inspectors observed the performance of the RP technicians with respect to all RP

work requirements. The inspectors evaluated whether technicians were aware of the

radiological conditions in their workplace and the RWP controls/limits, and whether their

performance was consistent with their training and qualifications with respect to the

radiological hazards and work activities.

16 Enclosure

The inspectors reviewed a maximum of 10 radiological problem reports since the last

inspection that found the cause of the event to be RP technician error. The inspectors

evaluated whether there was an observable pattern traceable to a similar cause. The

inspectors assessed whether this perspective matched the corrective action approach

taken by the licensee to resolve the reported problems.

b. Findings

No findings were identified.

2RS3 In-Plant Airborne Radioactivity Control and Mitigation (71124.03)

The inspection activities supplement those documented in IR 05000440/2010003, and

constitute one complete sample as defined in IP 71124.03-05.

.1 Inspection Planning (02.01)

a. Inspection Scope

The inspectors reviewed the plant USAR to identify areas of the plant designed as

potential airborne radiation areas and any associated ventilation systems or airborne

monitoring instrumentation. Instrumentation review included continuous air monitors

(continuous air monitors and particulate-iodine-noble-gas-type instruments) used to

identify changing airborne radiological conditions such that actions to prevent an

overexposure may be taken. The review included an overview of the respiratory

protection program and a description of the types of devices used.

The inspectors reviewed USAR, TS, and emergency planning documents to identify

location and quantity of respiratory protection devices stored for emergency use.

The inspectors reviewed the licensees procedures for maintenance, inspection, and use

of respiratory protection equipment including self-contained breathing apparatus

(SCBA). Additionally, the inspectors reviewed procedures for air quality maintenance

and the reported PIs to identify any related to unintended dose resulting from intakes of

radioactive materials.

b. Findings

No findings were identified.

.2 Engineering Controls (02.02)

a. Inspection Scope

The inspectors reviewed the licensees use of permanent and temporary ventilation to

determine whether the licensee used ventilation systems as part of its engineering

controls (in lieu of respiratory protection devices) to control airborne radioactivity. The

inspectors reviewed procedural guidance for use of installed plant systems, such as

containment purge, spent fuel pool ventilation, and auxiliary building ventilation, and

assessed whether the systems are used, to the extent practicable, during high-risk

activities (e.g., using containment purge during cavity flood up).

17 Enclosure

The inspectors selected installed ventilation systems used to mitigate the potential for

airborne radioactivity, and evaluated whether the ventilation airflow capacity, flow path

(including the alignment of the suction and discharges), and filter/charcoal unit

efficiencies, as appropriate, were consistent with maintaining concentrations of airborne

radioactivity in work areas below the concentrations of an airborne area to the extent

practicable.

The inspectors selected temporary ventilation system setups (HEPA/charcoal negative

pressure units, down draft tables, tents, metal Kelly buildings, and other enclosures)

used to support work in contaminated areas. The inspectors assessed whether the use

of these systems was consistent with licensee procedural guidance and as-low-as-is-

reasonably-achievable (ALARA) concepts.

b. Findings

No findings were identified.

.3 Use of Respiratory Protection Devices (02.03)

a. Inspection Scope

For those situations where it is impractical to employ engineering controls to minimize

airborne radioactivity, the inspectors assessed whether the licensee provided respiratory

protective devices such that occupational doses are ALARA. The inspectors selected

work activities where respiratory protection devices were used to limit the intake of

radioactive materials, and assessed whether the licensee performed an evaluation

concluding that further engineering controls were not practical and that the use of

respirators was ALARA. The inspectors also evaluated whether the licensee had

established means (such as routine bioassay) to determine if the level of protection

(protection factor) provided by the respiratory protection devices during use was at least

as good as that assumed in the licensees work controls and dose assessment.

The inspectors assessed whether respiratory protection devices used to limit the intake

of radioactive materials were certified by the National Institute for Occupational Safety

and Health/Mine Safety and Health Administration (NIOSH/MSHA) or have been

approved by the NRC in accordance with 10 CFR 20.1703(b). The inspectors selected

work activities where respiratory protection devices were used. The inspectors

evaluated whether the devices were used consistent with their NIOSH/MSHA

certification or any conditions of their NRC approval.

The inspectors reviewed records of air testing for supplied-air devices and SCBA bottles

to assess whether the air used in these devices meets or exceeds Grade D quality. The

inspectors reviewed plant breathing air supply systems to determine whether they meet

the minimum pressure and airflow requirements for the devices in use.

The inspectors selected individuals qualified to use respiratory protection devices, and

assessed whether they have been deemed fit to use the devices by a physician.

The inspectors selected several individuals assigned to wear a respiratory protection

device and observed them donning, doffing, and functionally checking the device as

appropriate. Through interviews with these individuals, the inspectors evaluated

whether they knew how to safely use the device and how to properly respond to any

18 Enclosure

device malfunction or unusual occurrence (loss of power, loss of air, etc.). The

inspectors reviewed training curricula for users of the devices.

The inspectors chose various respiratory protection devices staged and ready for use in

the plant or stocked for issuance. The inspectors assessed the physical condition of the

device components (mask or hood, harnesses, air lines, regulators, air bottles, etc.) and

reviewed records of routine inspection for each. The inspectors selected several of the

devices and reviewed records of maintenance on the vital components (e.g., pressure

regulators, inhalation/exhalation valves, hose couplings). The inspectors assessed

whether onsite personnel assigned to repair vital components had received vendor-

provided training.

b. Findings

No findings were identified.

.4 Self-Contained Breathing Apparatus for Emergency Use (02.04)

a. Inspection Scope

Based on USAR, TS, and emergency operating procedure requirements, the inspectors

reviewed the status and surveillance records of SCBAs staged in-plant for use during

emergencies. The inspectors reviewed the licensees capability for refilling and

transporting SCBA air bottles to and from the control room and operations support

center during emergency conditions.

The inspectors selected individuals on control room shift crews, and individuals from

designated departments currently assigned emergency duties (e.g., onsite search and

rescue duties) to assess whether control room operators and other emergency response

and RP personnel (assigned in-plant search and rescue duties or as required by

emergency operating procedures or the emergency plan) were trained and qualified in

the use of SCBAs (including personal bottle change out). The inspectors evaluated

whether personnel assigned to refill bottles were trained and qualified for that task.

The inspectors determined whether appropriate mask sizes and types were available for

use (i.e., in-field mask size and type matched what was used in fit-testing). The

inspectors selected various on-shift operators to determine whether they have no facial

hair that would interfere with the sealing of the mask to the face and whether vision

correction (e.g., glasses inserts or corrected lenses) were available as appropriate.

The inspectors reviewed the past 2 years of maintenance records for several SCBA

units used to support operator activities during accident conditions and designated as

ready for service to assess whether any maintenance or repairs on any SCBA units

vital components were performed by an individual, or individuals, certified by the

manufacturer of the device to perform the work. The vital components typically are the

pressure-demand air regulator and the low-pressure alarm. The inspectors reviewed the

onsite maintenance procedures governing vital component work to determine any

inconsistencies with the SCBA manufacturers recommended practices. For those

SCBAs designated as ready for service, the inspectors determined whether the

required, periodic air cylinder hydrostatic testing was documented and up to date, and

the retest air cylinder markings required by the U.S. Department of Transportation were

in place.

19 Enclosure

b. Findings

No findings were identified.

.5 Problem identification and Resolution (02.05)

a. Inspection Scope

The inspectors reviewed CRs and other corrective action documents to determine

whether problems associated with control and mitigation of in-plant airborne radioactivity

were being identified at the appropriate threshold and were properly addressed for

resolution in the licensees CAP.

b. Findings

No findings were identified

2RS4 Occupational Dose Assessment (71124.04)

This inspection constituted a partial sample as defined in IP 71124.04-05.

.1 Inspection Planning (02.01)

a. Inspection Scope

The inspectors reviewed the results of RP program audits related to internal and external

dosimetry (e.g., licensees quality assurance audits, self-assessments, or other

independent audits) to gain insights into overall licensee performance in the area of dose

assessment and focus the inspection activities consistent with the principle of smart

sampling.

b. Findings

No findings were identified.

.2 Internal Dosimetry (02.03)

Internal Dose Assessment - Airborne Monitoring

a. Inspection Scope

The inspectors reviewed the licensee's program for airborne radioactivity assessment

and dose assessment, as applicable, based on airborne monitoring and calculations of

derived air concentration. The inspectors determined whether flow rates and collection

times for air sampling equipment were adequate to allow lower limits of detection to be

obtained. The inspectors also reviewed the adequacy of procedural guidance to assess

internal dose if respiratory protection was used. The licensee had not performed dose

assessments using airborne/derived air concentration monitoring since the last

inspection.

20 Enclosure

b. Findings

No findings were identified.

.3 Special Dosimetric Situations (02.04)

Dosimeter Placement and Assessment of Effective Dose Equivalent for External

Exposures.

a. Inspection Scope

The inspectors reviewed the licensee's methodology for monitoring external dose in

non-uniform radiation fields or where large dose gradients exist. The inspectors

evaluated the licensee's criteria for determining when alternate monitoring, such as use

of multi-badging, was to be implemented.

The inspectors reviewed dose assessments performed using multi-badging to evaluate

whether the assessment was performed consistent with licensee procedures and

dosimetric standards.

b. Findings

No findings were identified.

4. OTHER ACTIVITIES

4OA1 Performance Indicator Verification (71151)

.1 Mitigating Systems Performance Index - Heat Removal System

a. Inspection Scope

The inspectors sampled licensee submittals for the Mitigating Systems Performance

Index (MSPI) - Heat Removal System performance indicator for the period from the third

quarter 2009 through the second quarter 2010. To determine the accuracy of the PI

data reported during those periods, PI definitions and guidance contained in the Nuclear

Energy Institute (NEI) Document 99-02, Regulatory Assessment Performance Indicator

Guideline, Revision 6, dated October 2009, were used. The inspectors reviewed the

licensees operator narrative logs, issue reports, event reports, MSPI derivation reports,

and NRC Integrated Inspection Reports for the period of the third quarter 2009 through

the second quarter 2010 to validate the accuracy of the submittals. The inspectors

reviewed the MSPI component risk coefficient to determine if it had changed by more

than 25 percent in value since the previous inspection, and if so, that the change was in

accordance with applicable NEI guidance. The inspectors also reviewed the licensees

issue report database to determine if any problems had been identified with the PI data

collected or transmitted for this indicator and none were identified. Documents reviewed

are listed in the Attachment to this report.

This inspection constituted one MSPI heat removal system sample as defined in

IP 71151-05.

21 Enclosure

b. Findings

No findings of significance were identified.

.2 Mitigating Systems Performance Index - Residual Heat Removal System

a. Inspection Scope

The inspectors sampled licensee submittals for the MSPI - Residual Heat Removal

System performance indicator for the period from the third quarter 2009 through the

second quarter 2010. To determine the accuracy of the PI data reported during those

periods, PI definitions and guidance contained in the Nuclear Energy Institute (NEI)

Document 99-02, Regulatory Assessment Performance Indicator Guideline,

Revision 6, dated October 2009, were used. The inspectors reviewed the licensees

operator narrative logs, issue reports, MSPI derivation reports, event reports and NRC

Integrated Inspection Reports for the period of the third quarter 2009 through the second

quarter 2010 to validate the accuracy of the submittals. The inspectors reviewed the

MSPI component risk coefficient to determine if it had changed by more than 25 percent

in value since the previous inspection, and if so, that the change was in accordance with

applicable NEI guidance. The inspectors also reviewed the licensees issue report

database to determine if any problems had been identified with the PI data collected or

transmitted for this indicator and none were identified. Documents reviewed are listed in

the Attachment to this report.

This inspection constituted one MSPI residual heat removal system sample as defined in

IP 71151-05.

b. Findings

No findings of significance were identified.

.2 Mitigating Systems Performance Index - Cooling Water Systems

a. Inspection Scope

The inspectors sampled licensee submittals for the MSPI - Cooling Water Systems

performance indicator for the period from the third quarter 2009 through the second

quarter 2010. To determine the accuracy of the PI data reported during those periods,

PI definitions and guidance contained in the NEI Document 99-02, Regulatory

Assessment Performance Indicator Guideline, Revision 6, dated October 2009, were

used. The inspectors reviewed the licensees operator narrative logs, issue reports,

MSPI derivation reports, event reports and NRC Integrated Inspection Reports for the

period of the third quarter 2009 through the second quarter 2010 to validate the

accuracy of the submittals. The inspectors reviewed the MSPI component risk

coefficient to determine if it had changed by more than 25 percent in value since the

previous inspection, and if so, that the change was in accordance with applicable NEI

guidance. The inspectors also reviewed the licensees issue report database to

determine if any problems had been identified with the PI data collected or transmitted

for this indicator and none were identified. Documents reviewed are listed in the

Attachment to this report.

22 Enclosure

This inspection constituted one MSPI cooling water system sample as defined in

IP 71151-05.

b. Findings

No findings of significance were identified.

4OA2 Problem Identification and Resolution (71152)

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness, Public Radiation Safety, Occupational Radiation Safety, and

Physical Protection

.1 Routine Review of Items Entered Into the CAP

a. Inspection Scope

As part of the various baseline inspection procedures discussed in previous sections of

this report, the inspectors routinely reviewed issues during baseline inspection activities

and plant status reviews to verify that they were being entered into the licensees CAP at

an appropriate threshold, that adequate attention was being given to timely corrective

actions, and that adverse trends were identified and addressed. Attributes reviewed

included: identification of the problem was complete and accurate; timeliness was

commensurate with the safety significance; evaluation and disposition of performance

issues, generic implications, common causes, contributing factors, root causes,

extent-of-condition reviews, and previous occurrences reviews were proper and

adequate; and that the classification, prioritization, focus, and timeliness of corrective

actions were commensurate with safety and sufficient to prevent recurrence of the issue.

Minor issues entered into the licensees CAP as a result of the inspectors observations

are included in the Attachment to this report.

These routine reviews for the identification and resolution of problems did not constitute

any additional inspection samples. Instead, by procedure they were considered an

integral part of the inspections performed during the quarter and documented in

Section 1 of this report.

b. Findings

No findings were identified.

.2 Daily Corrective Action Program Reviews

a. Inspection Scope

In order to assist with the identification of repetitive equipment failures and specific

human performance issues for follow-up, the inspectors performed a daily screening of

items entered into the licensees CAP. This review was accomplished through

inspection of the stations daily CR packages.

These daily reviews were performed by procedure as part of the inspectors daily plant

status monitoring activities and, as such, did not constitute any separate inspection

samples.

23 Enclosure

b. Findings

No findings were identified.

.3 Semi-Annual Trend Review

a. Inspection Scope

The inspectors performed a review of the licensees CAP and associated documents to

identify trends that could indicate the existence of a more significant safety issue. The

inspectors review was focused on repetitive equipment issues, but also considered the

results of daily inspector CAP item screening discussed in Section 4OA2.2 above,

licensee trending efforts, and licensee human performance results. The inspectors

review nominally considered the 6-month period from January 2010 through June 2010,

although some examples expanded beyond those dates where the scope of the trend

warranted.

The reviews also included issues documented outside of the normal CAP in major

equipment problem lists, repetitive and/or rework maintenance lists, departmental

problem/challenges lists, system health reports, quality assurance audit/surveillance

reports, self-assessment reports, and maintenance rule assessments. The inspectors

compared and contrasted their results with the results contained in the licensees

CAP trending reports. Corrective actions associated with a sample of the issues

identified in the licensees trending reports were reviewed for adequacy.

This review constituted a single semi-annual trend inspection sample as defined in

IP 71152-05.

b. Findings

No findings were identified.

.4 In-depth Review- Technical Specifications Compliance

a. Inspection Scope

The inspectors performed an annual follow-up of selected issues sample of the

licensees process for performing and documenting TS compliance. The inspectors

reviewed documentation in the licensees CAP, official narrative operating logs and LCO

tracking module, for compliance with site-specific administrative, operational, and

licensing procedures specifically to assess for proper control and documentation of the

entry and exit of LCO Conditions and Required Actions. Documents reviewed are listed

in the Attachment to this report.

This review constituted one in-depth problem identification and resolution sample as

defined in IP 71152-05.

b. Findings

Introduction: The inspectors identified a finding of very low safety significance (Green)

and an associated NCV for the licensees failure to follow the requirements of TS

LCO 3.0.2 by not entering TS LCO 3.3.5.1 Condition A and TS 3.3.6.1 Condition A when

24 Enclosure

reactor vessel level instruments 1B21N0673C and 1B21N0674C were declared

inoperable. Technical Specification LCO 3.0.2 requires that Upon discovery of a failure

to meet an LCO, the Required Actions of the associated Conditions shall be met, except

as provided in LCO 3.0.5 and LCO 3.0.6.

Description: On August 9, 2010, during a review of operator narrative logs, the

inspectors noted a log entry that identified the use of a TS Surveillance Requirement

(SR) Note to support the performance of WO #200322765, PDP - New PM Replace

Rosemount STU Card. This WO included a step to acquire as-found data of the card

being replaced prior to its removal. The method of acquiring this as-found data included

performing portions of surveillance test procedure SVI-B21-T0187C, ECCS/HPCS RPV

Water Level 2 and Level 8 Channel C Functional for 1B21-N673C. Additionally, this WO

step stated, Sign Off/Close Surveillance Instruction as No Credit. Surveillance test

SVI-B21-T0187C renders Reactor Vessel Level instruments 1B21N0673C and

1B21N0674C inoperable. This surveillance references the TS Surveillance Notes

associated with SR 3.3.5.1 and 3.3.6.1. These SR Notes state, in part, When a channel

is placed in an inoperable status solely for performance of required Surveillances, entry

into associated Conditions and Required Actions may be delayed. The licensee utilized

the SR Note during the performance of as-found checks using the surveillance and did

not enter the Conditions and Required Actions for the 22 minutes it took to perform the

test.

The inspectors reviewed the licensees use of the surveillance notes and determined

that the delay in entering the Conditions and Required Actions was inappropriate

because the surveillance was being performed to satisfy WO requirements, not

TS-required SRs. As a result, the licensee declared the instruments inoperable but

did not enter the Conditions or Required Actions for the associated LCOs. This is

contrary to the requirements of TS LCO 3.0.2 which states Upon discovery of a failure

to meet an LCO, the Required Actions of the associated Conditions shall be met, except

as provided in LCO 3.0.5 and LCO 3.0.6. Limiting Condition of Operation 3.0.5 and

LCO 3.0.6 did not apply in this situation.

An additional review of recent narrative log entries identified several instances of

misapplication of the same surveillance notes. The longest time period the LCO was not

adhered to was 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> and 47 minutes. In combination with the replacement and

subsequent operability testing, the instrument(s) were inoperable on several different

occasions, for a sum total of 13 hours1.50463e-4 days <br />0.00361 hours <br />2.149471e-5 weeks <br />4.9465e-6 months <br /> and 29 minutes. The LCO allows the instrument(s)

to be inoperable for up to 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> before any additional actions are required. The

inspectors did not identify any instances where the LCO Required Action times were

exceeded.

Analysis: The inspectors determined that the licensees failure to follow TS LCO 3.0.2

constituted a performance deficiency. Specifically, the licensee did not enter the LCOs

and Required Actions for inoperable TS equipment. The inspectors evaluated the

performance deficiency in accordance with IMC 0612, Appendix B, Issue Screening.

This performance deficiency was not similar to any of the examples in IMC 0612,

Appendix EProperty "Inspection Manual Chapter" (as page type) with input value "NRC Inspection Manual 0612,</br></br>Appendix E" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process., Examples of Minor Issues," but was characterized as more than minor

because it impacted the Equipment Performance attribute of the Mitigating Systems

Cornerstone, and adversely affected the cornerstone objective to ensure the availability,

reliability, and capability of systems that respond to initiating events to prevent

undesirable consequences (i.e., core damage); and if left uncorrected it could lead to a

more significant safety concern.

25 Enclosure

The inspectors determined the finding could be evaluated using the SDP in accordance

with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 -

Initial Screening and Characterization of findings, Table 3b for the Mitigating Systems

Cornerstone. The inspectors determined the finding was of very low safety significance

(Green) because it was not a design/qualification deficiency, did not represent a loss of

system safety function, did not result in a loss of function of a single train for greater than

its TS-allowable outage time, did not result in a loss of function of nonsafety-related

risk-significant equipment and was not risk significant due to external events.

This finding has a cross-cutting aspect in the decision making component of the Human

Performance cross-cutting area (per IMC 0310 H.1(b)), because the licensee did not use

conservative assumptions to ensure the proposed action was safe. Specifically, the

licensee incorrectly used the TS SR Note to satisfy maintenance requirements.

Enforcement: The inspectors determined that the finding represents a violation of

regulatory requirements because it involved improper implementation of TS. The

licensee utilized TS SR Notes while performing surveillances to satisfy maintenance

WOs. In accordance with TS LCO 3.0.2, in these cases entry into TS LCO 3.3.5.1

Condition A and 3.3.6.1 Condition A is required. Contrary to the above, the licensee did

not enter the Conditions and Required Actions immediately upon declaring TS-required

instrumentation inoperable. Because this finding is of very low safety significance and

because it was entered into the licensees CAP as CR 10-81162, this violation is being

treated as an NCV consistent with Section 2.3.2 of the NRC Enforcement Policy.

(NCV 05000440/2010004-02; Failure to Comply with Technical Specification LCOs

When Reactor Vessel Level Instruments Were Declared Inoperable.)

4OA3 Follow-up of Events and Notices of Enforcement Discretion (71153)

.1 (Closed) Licensee Event Report 05000440/2010-003: Loss of Control Rod Drive Header

Pressure Results in Manual RPS Actuation

a. Inspection Scope

On May 11, 2010, a manual actuation of RPS was inserted to comply with TS because

of multiple accumulators being inoperable coincident with the inability to restore control

rod drive (CRD) charging header pressure. A trip unit failure caused an invalid

loss-of-coolant accident (LOCA) initiation signal and resulted in the load shed of the

XH12 stub bus. Due to an abnormal electrical lineup, both CRD pumps tripped and they

were unable to be restarted. The licensee replaced the trip unit and restored the CRD

system to its normal configuration. The licensee documented the failed equipment in

CR 10-76727. The inspectors reviewed this Licensee Event Report (LER) and did not

identify any findings or violations of NRC requirements. Documents reviewed as part of

this inspection are listed in the attachment. This LER is closed.

This event follow-up review constituted one sample as defined in IP 71153-05.

26 Enclosure

.2 (Closed) Retraction of Event Notification 45815: Loss of Safety Function to Control the

Release of Radioactive Material

a. Inspection Scope

On April 6, 2010, the licensee initiated an event notification (EN) related to a loss of

safety function involving five containment isolation valves. Specifically, the licensee

reported that they had a potential loss of safety function for the ability to control the

release of radioactive material. This was due to a loss of power to the LOCA isolation

logic associated with containment penetration single valve isolations. On June 6, 2010,

the licensee retracted this notification. The licensee evaluated the condition and

determined the containment penetrations were still able to perform their design function.

The inspectors reviewed the information contained in the evaluation, and did not identify

any findings or violations related to the licensees retraction. This EN retraction is

closed.

This event follow-up review constituted one sample as defined in IP 71153-05.

4OA5 Other Activities

.1 (Closed) Unresolved Item 05000440/2010003-06: Failure to Perform a Hydrostatic Test

in Accordance with ASME Code

a. Inspection Scope

This Unresolved Item (URI) is associated with the licensees actions following a repair to

ESW underground piping in the spring of 2009. The licensee conducted only a leak test

of the repairs rather than a hydrostatic test, and the coupling used to repair the pipe leak

was not hydrostatically tested for 10 minutes prior to installation in the system. After

further review of the repair process and interaction with the ASME code committee, the

inspectors determined that the Dresser coupling used to repair the pipe did not meet the

ASME code definition of a component, and was therefore not required to be

hydrostatically tested. This URI is closed and no further actions are required.

.2 Institute of Nuclear Power Operations Plant Assessment Report Review

a. Inspection Scope

The inspectors reviewed the final report for the Institute of Nuclear Power Operations

(INPO) plant assessment of Perry station conducted in August 2009. The inspectors

reviewed the report to ensure that issues identified were consistent with the NRC

perspectives of licensee performance and to verify whether any significant safety issues

were identified that required further NRC follow-up.

b. Findings

No findings of significance were identified.

27 Enclosure

4OA6 Meetings

.1 Exit Meeting

The inspectors presented the inspection results to the Site Vice-President,

Mr. Mark Bezilla, and other members of licensee management on October 6, 2010.

The inspectors asked the licensee whether any materials examined during the

inspection should be considered proprietary. No proprietary information was identified.

.2 Interim Exit Meetings

An interim exit meeting was conducted for radiological hazard assessment and exposure

controls, in-plant airborne radioactivity control and mitigation, and occupational dose

assessment with Mr. T. Jardine and other members of the Perry staff on July 16, 2010.

The inspectors confirmed that none of the potential report input discussed was

considered proprietary.

4OA7 Licensee-Identified Violations

The following violation of very low safety significance (Green) was identified by the

licensee and is a violation of NRC requirements which meets the criteria of the NRC

Enforcement Policy, for being dispositioned as an NCV.

  • On August 25, 2010, the licensee identified a failure to meet the requirements of TS 5.5.9, Diesel Fuel Oil Testing Program requirements by failing to conduct the test for

viscosity at the prescribed temperature when receiving new fuel oil. The cause was

a failure to make appropriate procedure changes when the site implemented a

license change request that revised this TS requirement. Specifically, in September

1990, when the license change request was implemented by the site, the

temperature specified in SR 3.8.3.3 changed from 100 °F to 40 °C. Following this

change, the site did not recognize that the fuel oil viscosity test procedures

containing the prescribed testing temperature needed to be changed to align with the

new TS requirements, and therefore, the procedures incorrectly continued to reflect

the temperature cited in the previous TS version. Licensee personnel had been

testing the fuel oil in accordance with these procedures for approximately 20 years.

Corrective actions include sampling of all three fuel storage tanks for the diesel

generators, testing the samples for viscosity at the correct temperature requirement,

and implementation of procedural changes to incorporate the revised temperature.

All other TS-required surveillances of fuel oil properties were properly performed and

completed as required to ensure current operability. The violation was determined to

be of low safety significance through a licensee evaluation of risk. The licensee

entered this performance deficiency into the CAP as CR 10-81724, Fuel Oil Samples

Not Analyzed per Tech Specs.

ATTACHMENT: SUPPLEMENTAL INFORMATION

28 Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

M. Bezilla, Vice President Nuclear

D. Evans, Work and Outage Management Director

J. Grabnar, Site Engineering Director

H. Hanson, Performance Improvement Director

T. Jardine, Operations Manager

K. Krueger, Plant General Manager

P. McNulty, Radiation Protection Manager

M. Stevens, Maintenance Director

J. Tufts, Chemistry Manager

Other

C. OClare, Ohio Department of Health

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED

Opened and Closed

05000440/2010004-01 NCV Unacceptable Preconditioning of RHR Valve Prior to ASME

In-Service Testing (1R22)05000440/2010004-02 NCV Failure to Comply with Technical Specification LCOs When

Reactor Vessel Level Instruments Were Declared

Inoperable (4OA2.4)

Closed

05000440/2010003-06 URI Failure to Hydrostatically Test Replacement Components in

Accordance with ASME (Section 4OA5.1)

05000440/2010-003 LER Loss of Control Rod Drive Header Pressure Results in

Manual RPS Actuation (Section 4OA3.1)

Discussed

45815 EN Retraction of Event Notification 45815: Loss of Safety

Function to Control the Release of Radioactive Material

(Section 4OA3.2)

1 Attachment

LIST OF DOCUMENTS REVIEWED

The following is a partial list of documents reviewed during the inspection. Inclusion on this list

does not imply that the NRC inspector reviewed the documents in their entirety, but rather that

selected sections or portions of the documents were evaluated as part of the overall inspection

effort. Inclusion of a document on this list does not imply NRC acceptance of the document or

any part of it, unless this is stated in the body of the inspection report.

1R01 Adverse Weather

CR 10-80444; Security Project - North-Side Concrete T Wall Installation Issues

Drawing 743-0013-00000; Topography and Storm Drain Composite; Revision D

EER 600631290; Perform Evaluation to Determine Locations of Drainage Gaps in Installed

T-Walls; dated August 4, 2010

1R04 Equipment Alignment

CR 08-42257; Annulus Exhaust Gas Treatment System (AGETS) "A" Train Low Flow

Adjustment; dated June 20, 2008

CR 10-72614; Unplanned Fire Suppression Impairment for Annulus Exhaust Gas Treatment

System; dated March 4, 2010

CR 08-34483; Annulus Exhaust Gas Treatment System Flow Indication Low Flow; dated

January 29, 2008

CR 07-31871; AEGTS B Discharge Damper Is Not Functioning Correctly; dated

December 21, 2007

Drawing 912-0605-00000; Reactor Building Annulus Exhaust Gas Treatment; Revision W

PYBP-POS-2-2; Annulus Exhaust Gas Treatment System A (B) Outage Protected Equipment

Posting Checklist; Revision 10

PNPP No. 10392; Annulus Exhaust Gas Treatment System A (B) Outage Protected Equipment

Posting Checklist; dated July 14, 2009

SOI-M15; AEGTS System; Revision 8

VLI-M23/24; MCC, Switchgear and Miscellaneous Electrical Equipment Area HVAC System;

Revision 7

CR 10-82114; 0M23C0002B Did Not Trip with a B Train Trip Signal Present; dated

September 2, 2010

CR 10-82118; Replacement Solenoid Valve Mount Screw Holes Are Not Threaded; dated

August 31, 2010

Drawing 912-0609-00000; MCC Switchgear and Misc Electrical Equipment Areas HVAC

System and Battery Room Exhaust; Revision AA

Perry Plant Health Report 2010-2 for P42 - Emergency Closed Cooling System

SOI-P42; Emergency Closed Cooling System; Revision 16

VLI-P42; Emergency Closed Cooling System; Revision 15

Drawing 302-0621-00000; Emergency Closed Cooling System; Revision SS

Drawing 208-0041-00002; Reactor Protection System MG Set S001B

Drawing 208-0041-00001; Reactor Protection System MG Set S001A

CR 10-81707; Overheating on Voltage Regulator for RPS MG Set B; dated August 25, 2010

2 Attachment

1R05 Fire Protection (Annual/Quarterly)

PAP-1910; Fire Protection Program; Revision 19

P54-24; Calculation of Combustible Loading and Allowable Limits for Fire Loading; Revision 4

FPI-0IB; Pre-Fire Plan Instruction - Intermediate Building; Revision 5

FPI-0CC; Pre-Fire Plan Instruction - Control Complex; Revision 8

CR 10-80981; Documentation of NRC Questions; dated August 9, 2010

CR 10-81985; Response to Questions from the NRC Resident Inspector; dated August 27, 2010

FPI-1AB; Pre-Fire Plan Instruction - Auxiliary Building; Revision 3

CR 10-82504; NRC Question Regarding Pen Seals in AX 620 West; dated September 10, 2010

1R06 Internal Flooding

PAP-0204; Housekeeping/Cleanliness Control Program; Revision 24

ARI-H13-P601-0018; Leak Detection; Revision 13

NOP-OP-1012; Material Readiness and Housekeeping Inspection Program; Revision 5

CR 10-77685; Various Through Wall Piping Leaks on N71; dated June 3, 2010

Drawing 911-0617; Auxiliary Building Drains; Revision F

1R11 Licensed Operator Requalification Program

PYBP-PTS-0005; Operator Continuing Training Program Administration; Revision 25

PYBP-POS-0027; Operator Actions from Memory; Revision 0, dated December 3, 2008

Simulator Exercise Guide OTLC-3058201010_PY_SGC1; Cycle 10 2010 Evaluated Scenario

C1; Revision 0

CR 10-80980; Unsat Training Observation - Ops Performance Improvement Time Not Properly

Used; dated August 9, 2010

CR 10-81725; Unqualified Individuals Signing as Training Coordinators; dated August 25, 2010

1R12 Maintenance Effectiveness

WO 200284303; Chg Oil Fltrs Combustion Gas Purge Unit; dated July 21, 2010

CR 10-79817; Wrong Oil Added to CGMC Reservoir; dated July 17, 2010

CR 10-80089; NRC-ID. No FME High Risk Brief Sheet in Work Order; dated July 22, 2010

CR 10-80169; Failed PMT for CGMC B Aux Oil Pump; dated July 24, 2010

Clearance EPY-M25-0005; Control Room HVAC Supply Plenum; dated September 1, 2010

LCOTR# A10-M25-032; M25/26 Inoperable, Period 5 Week 10; dated August 30, 2010

CR 10-81952; Relay Contacts do not Change State; dated August 30, 2010

CR 10-81957; Loose Fittings on Low Flow Switch; dated August 30, 2010

Drawing 912-0610-00000; Control Room HVAC and Emergency Recirculation System;

Revision FF

CR 10-82639; Maintenance HPCS Work Start Deficiencies; dated September 13, 2010

CR 10-82715; Inadequate Order for Div 3 Fuel Oil Day Tank Work; dated September 16, 2010

CR 10-82864; Grease Fitting Damaged during Disassembly; dated September 19, 2010

CR 10-82970; Less Than Adequate Contingency Planning for Div 3 DG Inspections; dated

September 21, 2010

CR 10-82989; FME Concerns Identified in Div 3 DG Room; dated September 20, 2010

CR 10-83194; PMT Could Not Be Worked as Written; dated September 24, 2010

WO 200430281; Rebuild Ball Valves to Small and Large Seals

CR 10-83134; Lower Airlock Door Air Supply Flex Hoses Possibly Defective

CR 10-82842; Lower Airlock Pneumatic System Pressure Drop Test Failed

3 Attachment

CR 10-76252; Lower Containment Airlock Reactor Door

CR 09-69338; Upper Containment Airlock Reactor Door

1R13 Maintenance Risk Assessments and Emergent Work Control

NOP-OP-1007; Risk Management; Revision 7

CR 10-80396; Perry Not Notified of Conservative Grid Ops; dated July 28, 2010

CR 10-81724; Finding - Fuel Oil Samples not Analyzed per Tech Specs; dated August 25, 2010

CR 10-81727; Diesel Fuel Oil Sample Analysis Completion Dates Inconsistent; dated August

25, 2010

CR 10-81733; Procedure Steps Signed as Performed Inappropriately; dated August 25, 2010

CR 10-82658; Water/Steam Leak From 1N27F505D (RFBP D Discharge Check Valve); dated

September 15, 2010

WO 200430709; Wire Wrap/Inject Inspection Flange; dated September 17, 2010

WO 200430710; Remove Insulation @ Valve; dated September 16, 2010

ECP 10-0570-000; Leak Sealant Device on Reactor Feedwater Booster Pump D Discharge

Check Valve (1N27F0505D); Revision 0

ECP 10-0570-001; Install and Inject Leak Sealant Device on Reactor Feedwater Booster Pump

D Discharge Check Valve (1N27F0505D); Revision 1

CR 10-82682; Div 3 DG Generator Inter Pole Side Plate Movement; dated September 15, 2010

CR 10-82992; Div 3 Diesel Generator - Migrating Exciter Field Core Plates; dated

September 22, 2010

WO 200430766; Remove Generator Rotor, Inspect for Loose Wedge Studs; dated

September 15, 2010

1R15 Operability Evaluations

CR 10-78672; 1M43 Agastat Relay Qualification Issue; dated June 22, 2010

CR 10-81023; M52 Turning Vanes Degraded; dated August 10, 2010

Prompt Functionality Assessment for Degraded TSC Ventilation Supply Fan Turning Vanes;

dated August 13, 2010

Prompt Operability Determination for Diesel Generator Building Ventilation Systems; dated

July 15, 2010

CR 10-81973; No Insulation Inside Plenum; dated August 30, 2010

eSOMS Narrative Logs dated September 2, 2010

Prompt Operability Determination for ECC to FPCC Heat Exchanger Bypass Valve Stroke Time

Testing Failure; August 24, 2010

CR 10-81623; OP42F0255B Failed Stroke Closed Test; dated August 23, 2010

1R18 Permanent/Temporary Modifications

Perry Plant Health Report 2010-2 for Temporary Modifications

NOP-CC-2003; Engineering Changes; Revision 14

NORM-CC-2001; Engineering Change Process Flowcharts; Revision 00

ECP 10-0020-0000; Reference Documents - Hot Surge Tank Low Level Alarm from Level

Transmitter Signal; Revision 0

ECP 10-0020-0001; Hot Surge Tank Low Level Alarm from Level Transmitter Signal; Revision 3

WO 200399695; Hot Surge Tank Low Level Alarm; dated May 15, 2010

NOBP-ER-3003-01; Temporary Modification Review Checklist; Revision 00

CR 09-67788; Host Surge Tank (HST) Level Low Alarm Locked In; dated November 15, 2009

Drawing 302-0081-00000; Feedwater; Revision BBB

4 Attachment

Drawing 302-0101-00000; Condensate System; Revision TT

Drawing 208-0149-00002; MDFP Auto Start Logic & RFBP Auto Start Logic; Revision S

CR 10-82802; Potential Single Failure Vulnerability with Hot Surge Tank Temp Mod; dated

September 16, 2010

1R19 Post-Maintenance Testing

SVI-B21-T0137F; ECCS Drywell Pressure High Channel F Functional for 1B21-N694F;

Revision 5

PTI-M23-P0005; Emergency Service Water Pump House Ventilation System Train B Damper

Stroking; Revision 5

WO 200323496; Replace Rosemount MTU Card; dated August 11, 2010

WO 200323644; Replace Keylock Control Switch 1B21C-S27A; dated August 4, 2010

WO 200340398; Replace and Perform Calibration Check of 1M15D0001B Instrumentation;

dated August 25, 2010

WO 200327715; Replace AEGT Fan B Motor; dated August 25, 2010

WO 200290571; Replace SLS/MTR/Oil Hydramotor at ESW B Outlet Damper; dated

September 6, 2010

WO 200333304; MERP - Replace Utility Station w/NUS; dated September 6, 2010

CR 10-81632; Temperature Switch Found Tripped; dated August 23, 2010

CR 10-81633; RFACR: Damaged Field Conductor to Motor; dated August 23, 2010

WO 200328863; Replace Cntrl Relays in EH1304 Cubicle; dated September 20, 2010

SOI-R22; Metal Clad Switchgear 5-15 KV; Revision 25

CR 10-82852; Unexpected Reading Obtained during Functional Testing; dated September 19,

2010

SVI-E22-T1319; Diesel Generator Start and Load Division 3; Revision 15

CR 10-83148; Div 3 Emergency Diesel Generator Failure to Start During Testing; dated

September 24, 2010

CR 10-83163; Generator Stator Temperature Monitor is Erratic and Unreliable; dated

September 24, 2010

CR 10-83181; Div 3 DG Additional Tagging Points Requested; dated September 24, 2010

1R22 Surveillance Testing

SVI-E12-T2001; RHR A Pump and Valve Operability Test; Revision 26

SVI-E12-T1194; LPCI Pump A Discharge Low Flow (Bypass) Channel Functional for 1E12-

N652A; Revision 8

SVI-E51-T2001; RCIC Pump and Valve Operability Test; Revision 32

CR 01-79624; NRC-Identified Concern for Pre-conditioning Valve During Surveillance Testing;

dated July 12, 2010

NOP-ER-3204; Inservice Testing Program; Revision 1

eSOMS Narrative Logs dated July 7-8, 2010

SVI-P45-T2002; ESW Pump B and Valve Operability Test; Revision 26

SVI-R10-T5227; Off-Site Power Availability Verification; Revision 2

5 Attachment

2RS1 Radiological Hazard Assessment and Exposure Controls

CR 09-56065; Containment Vessel Drywell Purge Degraded Flows Impacting Refuel Floor;

dated March 25, 2009

CR 09-57294; Boundary Exceeded Radiological Controlled Area (RCA); dated April 16, 2009

CR 09-60436; Dose Rates in the P5480405 Condensate Backwash Receiving Tanl Higher than

Expected; dated June 11, 2009

CR 09-62628; Radioactive Material Found Outside the RCA; dated August 2, 2009

CR 09-63398 and Associated Apparent Cause Evaluation; Platform Found Outside with Fixed

Contamination; dated August 18, 2009

CR 09-66069; RISB Radioactive Material Inventory Discrepancies; dated October 16, 2009

CR 10-76774; Radiological Issues Associated with Division 2 ECC LOCA Initiation; dated

May 11, 2010

CR-09-54403; RFO-12 Elevated Airborne Levels During Separator Lift; dated February 28, 2009

HPI-C0014; Radlock key Issue; Revision 01

HPI-H0004; Identification of Radioactive Materials and Release of Materials from RCAs;

Revision 22

HPI-K0009; Operation of the WARF, RISB and OSSC Yard; Revision 0

HPI-L0004; Source Control Documentation and Inventory; Revision 8

NOPB-NF-3102; Control of Non-Special Nuclear Material in the Fuel Pools; Revision 00

NOP-OP-4101; Access Controls for Radiologically Controlled Areas; Revision 01

NOP-OP-4102; Radiological Postings, Labeling, and Markings; Revision 05

NOP-OP-4107; Radiation Work Permit; Revisions 4 and 5

NRC Form 748; National Source Tracking Transaction Report; dated January 12, 2009

NSTS Annual Inventory Reconciliation; dated September 9, 2009, and January 29, 2010

PNPP No. 10280; Sealed Source Leak Test Data Sheet HPI-L0004; dated January 13, 2010

PNPP No. 7445; Sealed Source Leak Test Data Sheet ORM 6.4.2; dated January 13, 2010

SVI-E31-T5190; Sealed Source Leak Test and Inventory; Revision 5

TEDE ALARA Evaluations for ALARA Plan Nos. 09-6018-02, 09-6041-00 and

10-0066; dates October 2008 and February 2010

2RS3 In-Plant Airborne Radioactivity Control and Mitigation

Air Sample Records/Collection and Evaluation Forms for Various Work Activities and Locations;

Various Dates in March and April 2009

CR 09-57025; Air Sampling Equipment Found with Expired Calibration; dated April 09, 2009

EP-Emergency Plan for Perry Nuclear Power Plant Docket Nos. 50-440; Revision 30

HPI-G0007; Maintenance of Respiratory Protective Equipment and Operation of the Respirator

Cleaning / Issue Facilities; Revision 21

HPI-G0008; Requalification of Respirators; Revision 07

HPI-L0003; Equipment History; Revision 06

HRI-0003; Respirator Qualification Health Assessment; Revision 02

NOP-OP-4301; Respiratory Protection Program; Revision 01

NOP-OP-4302; Issuing Respiratory Protection; Revision 00

NOP-OP-4303; Respirator Quantitative Fit Test Portacount PRO 8030; Revision 01

NOP-OP-4310; Firehawk M7 Self Contained Breathing Apparatus; Revision 04

NOP-OP-4702; Air Sampling; Revision 01

PSI-0022; Emergency Plan Training program; Revision 03

PYBP-RPS-0038; Radiologically Controlled Area HEPA Ventilation and HEPA Vacuum Unit

Program; Revision 01

6 Attachment

2RS4 Occupational Dose Assessment

ALARA Plan 09-6040; Suppression Pool Cleaning and Inspection; Revision 03

NOP-OP-4204; Special External Exposure Monitoring; Revision 03

NOP-OP-4204-04; Effective Dose Equivalent Dose Determination; Revision 01

NOP-OP-4205; Dose Assessment; Revision 03

NOP-OP-4206; Bioassay Program; Revision 00

NOP-OP-4503; Personnel Contamination Monitoring; Revision 02

Radiological Engineering Assessment; Source term Determination for Cycle 12 Operations;

Undated

RWP 09-6040; RFO-12 Suppression Pool Diving Activities; Revision 03

4OA1 Performance Indicator Verification

NOBP-LP-4012; NRC Performance Indicators; Revision 3

NOBP-LP-4012-06; MSPI Data Sheets for Heat Removal System from July 2009 to June 2010;

Revision 2

NOBP-LP-4012-07; MSPI Data Sheets for Residual Heat Removal System from July 2009 to

June 2010; Revision 2

NOBP-LP-4012-19; MSPI Data Sheets for Emergency Service Water from July 2009 to

June 2010; Revision 2

Mitigating Systems Performance Index Basis Document; Revision 4

PYBP-DES-0011; Mitigating Systems Performance Index; Revision 1

eSOMS Narrative Logs; July 2009 to June 2010

List of CRs for all MSPI monitored systems; July 2009 to June 2010

MSPI Derivation Reports for all MSPI monitored systems; June 2010

4OA2 Identification and Resolution of Problems

CRs for the period January 1, 2010, through June 30, 2010

CR 10-81162; Potential Misapplication of TS Note; dated August 12, 2010

eSOMS Narrative Logs; July 2010, to August 2010

eSOMS Action Tracking; July 2010 to August 2010

WO 200322765; PDP - New PM Replace Rosemount STU Card; dated August 9, 2010

SVI-B21-T0187C, ECCS/HPCS RPV Water Level 2 and Level 8 Channel C Functional for

1B21-N673C; Revision 6

4OA3 Follow-up of Events and Notices of Enforcement Discretion

LER 2010-003; Loss of Control Rod Drive Header Pressure Result in Manual RPS Actuation;

dated July 12, 2010

CR 10-74904; During SVI-E12T0146 Performance, Operations Received Unexpected

Annunciators; dated April 4, 2010

4OA7 Licensee-Identified Findings

CR 10-81724; Fuel Oil Samples not Analyzed per Tech Specs; dated August 25, 2010

7 Attachment

LIST OF ACRONYMS USED

AEGTS annulus exhaust gas treatment system

ALARA as-low-as-reasonably-achievable

ASME American Society of Mechanical Engineers

CAP corrective action program

CFR Code of Federal Regulations

CR condition report

ECC emergency closed cooling

EDG emergency diesel generator

ESW emergency service water

FENOC FirstEnergy Nuclear Operating Company

HEPA high-efficiency particulate air

HP health physics

HPCS high pressure core spray

HRA high radiation area

IMC Inspection Manual Chapter

IP Inspection Procedure

IR Inspection Report

IST inservice testing

LCO limiting condition for operation

LER Licensee Event Report

LPCI low pressure core injection

MSPI mitigating systems performance index

NCV non-cited violation

NEI Nuclear Energy Institute

NIOSH/MSSHA National Institute for Occupational Safety and Health/

Mine Safety and Health Administration

NOP Nuclear Operating Procedure

NRC Nuclear Regulatory Commission

ONI Off-Normal Instruction

PI performance indicator

PM post-maintenance

RCIC reactor core isolation cooling

RHR residual heat removal

RP radiation protection

RPS reactor protection system

RWP radiation work permit

SCBA self-contained breathing apparatus

SDP Significance Determination Process

SR surveillance requirement

SSC structure, system, or component

SVI Surveillance Instruction

TS Technical Specification

USAR Updated Safety Analysis Report

VHRA very high radiation area

WO work order

8 Attachment

M. Bezilla -2-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its

enclosure will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records (PARS) component of NRC's document system

(ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html

(the Public Electronic Reading Room).

Sincerely,

/RA/

Jamnes L. Cameron, Chief

Branch 6

Division of Reactor Projects

Docket No. 50-440

License No. NPF-58

Enclosure: Inspection Report 05000440/2010004

w/Attachment: Supplemental Information

cc w/encl: Distribution via ListServ

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OFFICE RIII RIII

NAME PVoss:dtp JCameron

DATE 10/28/10 10/29/10

OFFICIAL RECORD COPY

Letter to M. Bezilla from J. Cameron dated October 29, 2010

SUBJECT: PERRY NUCLEAR POWER PLANT NRC INTEGRATED

INSPECTION REPORT 05000440/2010004

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