IR 05000456/2008002: Difference between revisions
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| issue date = 05/15/2008 | | issue date = 05/15/2008 | ||
| title = IR 05000456-08-002, 05000457-08-002; on 1/01/2008 - 03/31/2008; Exelon Nuclear Generating Company, LLC; Braidwood Station Units 1 & 2; Surveillance Testing | | title = IR 05000456-08-002, 05000457-08-002; on 1/01/2008 - 03/31/2008; Exelon Nuclear Generating Company, LLC; Braidwood Station Units 1 & 2; Surveillance Testing | ||
| author name = Skokowski R | | author name = Skokowski R | ||
| author affiliation = NRC/RGN-III/DRP | | author affiliation = NRC/RGN-III/DRP | ||
| addressee name = Pardee C | | addressee name = Pardee C | ||
| addressee affiliation = Exelon Generation Co, LLC | | addressee affiliation = Exelon Generation Co, LLC | ||
| docket = 05000456, 05000457 | | docket = 05000456, 05000457 | ||
| Line 19: | Line 19: | ||
=Text= | =Text= | ||
{{#Wiki_filter: | {{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION REGION III 2443 WARRENVILLE ROAD, SUITE 210 LISLE, IL 60532-4352 May 15, 2008 Mr. Charles Chief Nuclear Officer and Senior Vice President Exelon Generation Company, LLC 4300 Winfield Road Warrenville, IL 60555 SUBJECT: BRAIDWOOD STATION, UNITS 1 AND 2 NRC INTEGRATED INSPECTION REPORT 05000456/2008002; 05000457/2008002 | ||
Mr. Charles Chief Nuclear Officer and Senior Vice President Exelon Generation Company, LLC 4300 Winfield Road Warrenville, IL 60555 | |||
SUBJECT: BRAIDWOOD STATION, UNITS 1 AND 2 NRC INTEGRATED INSPECTION REPORT 05000456/2008002; 05000457/2008002 | |||
==Dear Mr. Pardee:== | ==Dear Mr. Pardee:== | ||
On March 31, 2008 the U.S. Nuclear Regulatory Commission (NRC) completed an integrated inspection at your Braidwood Station, Units 1 and 2. The enclosed report documents the inspection results, which were discussed on April 10, 2008, with Mr. B. Hanson and other members of your staff. The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. Based on the results of this inspection, one NRC-identified finding of very low safety significance was identified. The finding involved a violation of NRC requirements. In addition, one licensee identified violation which was determined to be of very low safety significance is listed in this report. Because of the very low safety significance, and because these issues were entered into your corrective action program, the NRC is treating these issues as Non-Cited Violations in accordance with Section VI. A. 1 of the NRC Enforcement Policy. If you contest the subject or severity of a Non-Cited Violation, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector Office at the Braidwood Station. In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be made available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). | On March 31, 2008 the U.S. Nuclear Regulatory Commission (NRC) completed an integrated inspection at your Braidwood Station, Units 1 and 2. The enclosed report documents the inspection results, which were discussed on April 10, 2008, with Mr. B. Hanson and other members of your staff. The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. Based on the results of this inspection, one NRC-identified finding of very low safety significance was identified. The finding involved a violation of NRC requirements. In addition, one licensee identified violation which was determined to be of very low safety significance is listed in this report. Because of the very low safety significance, and because these issues were entered into your corrective action program, the NRC is treating these issues as Non-Cited Violations in accordance with Section VI. A. 1 of the NRC Enforcement Policy. If you contest the subject or severity of a Non-Cited Violation, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector Office at the Braidwood Station. In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be made available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). | ||
Sincerely,/RA/ Richard A. Skokowski, Chief Branch 3 Division of Reactor Projects Docket Nos. 50-456; 50-457 License Nos. NPF-72; NPF-77 | Sincerely, | ||
/RA/ Richard A. Skokowski, Chief Branch 3 Division of Reactor Projects Docket Nos. 50-456; 50-457 License Nos. NPF-72; NPF-77 Enclosure: Inspection Report 05000456/2008002; and 05000457/2008002 w/Attachment: Supplemental Information cc w/encl: Site Vice President - Braidwood Station Plant Manager - Braidwood Station Regulatory Assurance Manager - Braidwood Station Chief Operating Officer and Senior Vice President Senior Vice President - Midwest Operations Senior Vice President - Operations Support Vice President - Licensing and Regulatory Affairs Director - Licensing and Regulatory Affairs Manager Licensing - Braidwood, Byron and LaSalle Associate General Counsel Document Control Desk - Licensing Assistant Attorney General Illinois Emergency Management Agency J. Klinger, State Liaison Officer Chairman, Illinois Commerce Commission | |||
Inspection Report 05000456/2008002; and 05000457/2008002 | |||
Supplemental Information cc w/encl: Site Vice President - Braidwood Station Plant Manager - Braidwood Station Regulatory Assurance Manager - Braidwood Station Chief Operating Officer and Senior Vice President Senior Vice President - Midwest Operations Senior Vice President - Operations Support Vice President - Licensing and Regulatory Affairs Director - Licensing and Regulatory Affairs Manager Licensing - Braidwood, Byron and LaSalle Associate General Counsel Document Control Desk - Licensing Assistant Attorney General Illinois Emergency Management Agency J. Klinger, State Liaison Officer Chairman, Illinois Commerce Commission | |||
=SUMMARY OF FINDINGS= | =SUMMARY OF FINDINGS= | ||
| Line 64: | Line 54: | ||
==REACTOR SAFETY== | ==REACTOR SAFETY== | ||
===Cornerstone: | ===Cornerstone: Initiating Events, Mitigating Systems, and Barrier Integrity | ||
Initiating Events, Mitigating Systems, and Barrier Integrity | |||
{{a|1R01}} | {{a|1R01}} | ||
==1R01 Adverse Weather Protection== | ==1R01 Adverse Weather Protection== | ||
{{IP sample|IP=IP 71111.01}} | {{IP sample|IP=IP 71111.01}} | ||
===.1 Readiness For Impending Adverse Weather Condition - Heavy Rainfall/External Flooding Conditions=== | ===.1 Readiness For Impending Adverse Weather Condition - Heavy Rainfall/External Flooding Conditions=== | ||
=== | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
| Line 286: | Line 276: | ||
No findings of significance were identified. | No findings of significance were identified. | ||
===Cornerstone: | ===Cornerstone: Emergency Preparedness [EP] | ||
Emergency Preparedness [EP] | |||
{{a|1EP6}} | {{a|1EP6}} | ||
==1EP6 Drill Evaluation== | ==1EP6 Drill Evaluation== | ||
{{IP sample|IP=IP 71114.06}} | {{IP sample|IP=IP 71114.06}} | ||
===.1 Emergency Preparedness Drill Observation=== | ===.1 Emergency Preparedness Drill Observation=== | ||
=== | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
| Line 301: | Line 291: | ||
==RADIATION SAFETY== | ==RADIATION SAFETY== | ||
===Cornerstone: | ===Cornerstone: Occupational Radiation Safety 2OS3 Radiation Monitoring Instrumentation and Protective Equipment (71121.03) | ||
Occupational Radiation Safety 2OS3 Radiation Monitoring Instrumentation and Protective Equipment (71121.03) | |||
===.1 Inspection Planning=== | ===.1 Inspection Planning=== | ||
=== | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
| Line 538: | Line 528: | ||
===Closed=== | ===Closed=== | ||
: 05000456/2007-003-00 LER Improper Installation of Insulation on the Unit 1 Main Steam Safety Valves (Section 4OA3.3) | |||
Attachment | |||
==LIST OF DOCUMENTS REVIEWED== | ==LIST OF DOCUMENTS REVIEWED== | ||
The following is a partial list of documents reviewed during the inspection. | The following is a partial list of documents reviewed during the inspection. | ||
: Inclusion on this list does not imply that the NRC inspector reviewed the documents in their entirety, but rather that selected sections or portions of the documents were evaluated as part of the overall inspection effort. | : Inclusion on this list does not imply that the NRC inspector reviewed the documents in their entirety, but rather that selected sections or portions of the documents were evaluated as part of the overall inspection effort. | ||
: Inclusion of a document on this list does not imply NRC acceptance of the document or any part of it, unless this is stated in the body of the inspection report. | : Inclusion of a document on this list does not imply NRC acceptance of the document or any part of it, unless this is stated in the body of the inspection report. | ||
}} | }} | ||
Revision as of 11:10, 12 July 2019
| ML081360434 | |
| Person / Time | |
|---|---|
| Site: | Braidwood |
| Issue date: | 05/15/2008 |
| From: | Richard Skokowski Division Reactor Projects III |
| To: | Pardee C Exelon Generation Co |
| References | |
| FOIA/PA-2010-0209 IR-08-002 | |
| Download: ML081360434 (41) | |
Text
UNITED STATES NUCLEAR REGULATORY COMMISSION REGION III 2443 WARRENVILLE ROAD, SUITE 210 LISLE, IL 60532-4352 May 15, 2008 Mr. Charles Chief Nuclear Officer and Senior Vice President Exelon Generation Company, LLC 4300 Winfield Road Warrenville, IL 60555 SUBJECT: BRAIDWOOD STATION, UNITS 1 AND 2 NRC INTEGRATED INSPECTION REPORT 05000456/2008002; 05000457/2008002
Dear Mr. Pardee:
On March 31, 2008 the U.S. Nuclear Regulatory Commission (NRC) completed an integrated inspection at your Braidwood Station, Units 1 and 2. The enclosed report documents the inspection results, which were discussed on April 10, 2008, with Mr. B. Hanson and other members of your staff. The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. Based on the results of this inspection, one NRC-identified finding of very low safety significance was identified. The finding involved a violation of NRC requirements. In addition, one licensee identified violation which was determined to be of very low safety significance is listed in this report. Because of the very low safety significance, and because these issues were entered into your corrective action program, the NRC is treating these issues as Non-Cited Violations in accordance with Section VI. A. 1 of the NRC Enforcement Policy. If you contest the subject or severity of a Non-Cited Violation, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector Office at the Braidwood Station. In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be made available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/RA/ Richard A. Skokowski, Chief Branch 3 Division of Reactor Projects Docket Nos. 50-456; 50-457 License Nos. NPF-72; NPF-77 Enclosure: Inspection Report 05000456/2008002; and 05000457/2008002 w/Attachment: Supplemental Information cc w/encl: Site Vice President - Braidwood Station Plant Manager - Braidwood Station Regulatory Assurance Manager - Braidwood Station Chief Operating Officer and Senior Vice President Senior Vice President - Midwest Operations Senior Vice President - Operations Support Vice President - Licensing and Regulatory Affairs Director - Licensing and Regulatory Affairs Manager Licensing - Braidwood, Byron and LaSalle Associate General Counsel Document Control Desk - Licensing Assistant Attorney General Illinois Emergency Management Agency J. Klinger, State Liaison Officer Chairman, Illinois Commerce Commission
SUMMARY OF FINDINGS
IR 05000456/2008002, 05000457/2008002; 01/01/2008 - 03/31/2008; Braidwood Station Units 1 & 2; Surveillance Testing. This report covers a three-month period of inspection by resident inspectors and announced baseline inspections by regional inspectors.
One Green finding was identified by the inspectors. The finding was considered a Non-Cited Violation of NRC regulations. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review.
The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006.
A. NRC-Identified and Self-Revealing Findings
Cornerstone: Barrier Integrity
- Green.
A finding of very low safety significance and associated Non-Cited Violation of 10 CFR 50, Appendix B, Criterion V, Instructions Procedures and Drawings was identified by the inspectors for the licensee's failure to establish adequate acceptance criteria when performing a surveillance required by the plant's Technical Specifications. Specifically, acceptance criteria ensuring airflow flow from areas of low potential contamination to areas of high potential contamination when performing Technical Specification Surveillance Requirement 3.7.12.4 associated with the nonaccessible area exhaust filter plenum ventilation system in the auxiliary building was not established. The licensee has entered the issue into its corrective action program and intend establish qualitative criteria verifying air flow into spaces containing potential contaminated fluids during post accident conditions. This finding was more than minor because it affected the radiological barrier functionality of the control room and auxiliary building attribute under the barrier integrity cornerstone. The finding was of very low safety significance because all the answers were no to the SDP screening associated with the Barrier's Cornerstone. (Section 1R22)
B. Licensee-Identified Violations
A violation of very low safety significance that was identified by the licensee has been reviewed by the inspectors. Corrective actions planned or taken by the licensee have been entered into the licensee's corrective action program. This violation and corrective action tracking numbers are listed in Section 4OA7 of this report.
REPORT DETAILS
Summary of Plant Status
Unit 1 started the inspection period at full power. On January 8, 2008 power was reduced to 70 percent when control rod J-13 dropped into the core. Power was further reduced to 39 percent on January 9, 2008 to support control rod recovery. Unit 1 was restored to full power on January 12, 2008. On February 1, 2008, the licensee reduced power to 16 percent in order to access containment and vent and sample the 1C reactor coolant pump lower oil reservoir in order to clear a high oil level condition in the reservoir. Unit 1 was returned to full power on February 3, 2008 where it remained through the rest of the inspection period.
Unit 2 was operated at full power until February 14, 2008 when power was lowered to approximately 50 percent after the 2B main feed pump was tripped due to a hydraulic fluid leak in the pumps electro-hydraulic control system. Unit 2 was returned to full power on February 18, 2008, and remained at full power through the remainder of the inspection period.
REACTOR SAFETY
===Cornerstone: Initiating Events, Mitigating Systems, and Barrier Integrity
1R01 Adverse Weather Protection
.1 Readiness For Impending Adverse Weather Condition - Heavy Rainfall/External Flooding Conditions
=
a. Inspection Scope
The inspectors reviewed licensee preparations for impending heavy rainfall with the potential for external flooding conditions. Drainage ditches were verified clear of obstruction and flood barriers were confirmed in place. In addition, the inspectors walked down power block areas previously susceptible to ground water intrusion following heavy rainfall conditions to ensure no adverse impact on safety related equipment was sustained. Documents reviewed are listed in the Attachment to this report. This inspection constituted one readiness for impending adverse weather condition sample as defined in Inspection Procedure 71111.01
b. Findings
No findings of significance were identified.
1R04 Equipment Alignment
.1 Quarterly Partial System Walkdowns
a. Inspection Scope
The inspectors performed partial system walkdowns of the following risk-significant systems:
- 1A essential service water train;
- 2A residual heat removal train; and
- Unit 0 and Unit 1 component cooling water trains. The inspectors selected these systems based on their risk significance relative to the reactor safety cornerstones at the time they were inspected. The inspectors attempted to identify any discrepancies that could impact the function of the system, and, therefore, potentially increase risk. The inspectors reviewed applicable operating procedures, system diagrams, Updated Final Safety Analysis Report (UFSAR), Technical Specification (TS) requirements, Administrative TS, outstanding work orders, condition reports, and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have rendered the systems incapable of performing their intended functions. The inspectors also walked down accessible portions of the systems to verify system components and support equipment were aligned correctly and operable. The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no obvious deficiencies. The inspectors also verified that the licensee had properly identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the corrective action program with the appropriate significance characterization. Documents reviewed are listed in the Attachment. These activities constituted three partial system walkdown sample as defined by Inspection Procedure 71111.04.
b. Findings
No findings of significance were identified.
.2 Semi-Annual Complete System Walkdown
a. Inspection Scope
On January 20, 2008, the inspectors performed a complete system alignment inspection of the Unit 1 residual heat removal system to verify the functional capability of the system. This system was selected because it was considered both safety-significant and risk-significant in the licensee's probabilistic risk assessment. In addition, the licensee was preparing to perform maintenance that could require plant shutdown and cooldown to Mode 5, and required the residual heat removal system to perform its shutdown cooling function for reactor decay heat removal. The inspectors walked down the system to review mechanical and electrical equipment line-ups, electrical power availability, system pressure and temperature indications, as appropriate, component labeling, component lubrication, component and equipment cooling, hangers and supports, operability of support systems, and to ensure that ancillary equipment or debris did not interfere with equipment operation. A review of a sample of past and outstanding work orders was performed to determine whether any deficiencies significantly affected the system function. In addition, the inspectors reviewed the corrective action program (CAP) database to ensure that system equipment alignment problems were being identified and appropriately resolved. The documents used for the walkdown and issue review are listed in the Attachment.
4 Enclosure These activities constituted one complete system walkdown sample as defined by Inspection Procedure 71111.04.
b. Findings
No findings of significance were identified.
1R05 Fire Protection
.1 Routine Resident Inspector Tours
a. Inspection Scope
The inspectors conducted fire protection walkdowns which were focused on availability, accessibility, and the condition of firefighting equipment in the following risk-significant plant areas:
- 1A centrifugal charging pump room (fire zone 11.3D-1);
- 1B centrifugal charging pump room (fire zone 11.3G-1);
- 2A centrifugal charging pump room (fire zone 11.3D-2);
- 2B centrifugal charging pump room (fire zone 11.3G-2); and
- review of fire barrier integrity in spaces protected by gaseous suppression systems. The inspectors reviewed areas to assess if the licensee had implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant, effectively maintained fire detection and suppression capability, maintained passive fire protection features in good material condition, and had implemented adequate compensatory measures for out of service, degraded or inoperable fire protection equipment, systems, or features in accordance with the licensee's fire plan. The inspectors selected fire areas based on their overall contribution to internal fire risk as documented in the plant's Individual Plant Examination of External Events with later additional insights, their potential to impact equipment which could initiate or mitigate a plant transient, or their impact on the plant's ability to respond to a security event. Using the documents listed in the Attachment, the inspectors verified that fire hoses and extinguishers were in their designated locations and available for immediate use; that fire detectors and sprinklers were unobstructed, that transient material loading was within the analyzed limits; and fire doors, dampers, and penetration seals appeared to be in satisfactory condition. The inspectors also verified that minor issues identified during the inspection were entered into the licensee's corrective action program. These activities constituted five quarterly fire protection inspection samples as defined by Inspection Procedure 71111.05.
b. Findings
No findings of significance were identified.
5 Enclosure
.2 Annual Fire Protection Drill Observation
a. Inspection Scope
On March 12, 2008, the inspectors observed fire brigade activation when the control room was informed of a simulated fire emanating from the B train control room ventilation chiller. The observation evaluated the readiness of the plant fire brigade to fight fires. The inspectors verified that the licensee staff identified deficiencies; openly discussed them in a self-critical manner at the drill debrief, and took appropriate corrective actions. Specific attributes evaluated were:
- (1) proper wearing of turnout gear and self-contained breathing apparatus;
- (2) proper use and layout of fire hoses;
- (3) employment of appropriate fire fighting techniques;
- (4) sufficient firefighting equipment brought to the scene;
- (5) effectiveness of fire brigade leader communications, command, and control;
- (6) search for victims and propagation of the fire into other plant areas;
- (7) smoke removal operations;
- (8) utilization of pre planned strategies;
- (9) adherence to the pre planned drill scenario; and
- (10) drill objectives. Documents reviewed are listed in the Attachment to this report. These activities constituted one annual fire protection inspection sample as defined by Inspection Procedure 71111.05.
b. Findings
No findings of significance were identified.
1R11 Licensed Operator Requalification Program
.1 Resident Inspector Quarterly Review
a. Inspection Scope
On March 4, 2008, the inspectors observed two crews of licensed operators in the plant's simulator during licensed operator requalification examinations to verify that operator performance was adequate, evaluators were identifying and documenting crew performance problems and training was being conducted in accordance with licensee procedures. The inspectors evaluated the following areas:
- licensed operator performance;
- crew's clarity and formality of communications;
- ability to take timely actions in the conservative direction;
- prioritization, interpretation, and verification of annunciator alarms;
- correct use and implementation of abnormal and emergency procedures;
- control board manipulations;
- oversight and direction from supervisors; and
- ability to identify and implement appropriate TS actions and Emergency Plan actions and notifications. The crew performance in these areas was compared to pre-established operator action expectations and successful critical task completion requirements. Documents reviewed are listed in the Attachment to this report.
6 Enclosure This inspection constituted one quarterly licensed operator requalification program sample as defined in Inspection Procedure 71111.11.
b. Findings
No findings of significance were identified.
1R12 Maintenance Effectiveness
.1 Routine Quarterly Evaluations
a. Inspection Scope
The inspectors evaluated degraded performance issues involving the following risk significant systems:
- Units 1 and 2 auxiliary feedwater; and
- instrumentation and control systems. The inspectors reviewed events such as where ineffective equipment maintenance has resulted in valid or invalid automatic actuations of engineered safeguards systems and independently verified the licensee's actions to address system performance or condition problems in terms of the following:
- implementing appropriate work practices;
- identifying and addressing common cause failures;
- scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;
- characterizing system reliability issues for performance;
- charging unavailability for performance;
- trending key parameters for condition monitoring;
- ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and
- verifying appropriate performance criteria for structures, systems, and components/functions classified as (a)(2) or appropriate and adequate goals and corrective actions for systems classified as (a)(1). The inspectors assessed performance issues with respect to the reliability, availability, and condition monitoring of the system. In addition, the inspectors verified maintenance effectiveness issues were entered into the corrective action program with the appropriate significance characterization. Documents reviewed are listed in the Attachment. This inspection constituted two quarterly maintenance effectiveness samples as defined in Inspection Procedure 71111.12.
b. Findings
No findings of significance were identified.
7 Enclosure
1R13 Maintenance Risk Assessments and Emergent Work Control
a. Inspection Scope
The inspectors reviewed the licensee's evaluation and management of plant risk for the maintenance and emergent work activities affecting risk-significant and safety-related equipment listed below to verify that the appropriate risk assessments were performed prior to removing equipment for work:
- response to drop of Unit 1 Control Rod J-13;
- 1C reactor coolant pump lower motor bearing oil reservoir high level;
- 2A residual heat removal train online work window; and
- 1B diesel generator fuel supply line leak due to fretting failure. These activities were selected based on their potential risk significance relative to the reactor safety cornerstones. As applicable for each activity, the inspectors verified that risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate and complete. When emergent work was performed, the inspectors verified that the plant risk was promptly reassessed and managed. The inspectors reviewed the scope of maintenance work, discussed the results of the assessment with the licensee's probabilistic risk analyst or shift technical advisor, and verified plant conditions were consistent with the risk assessment. The inspectors also reviewed TS requirements and walked down portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met. Documents reviewed are listed in the Attachment to this report. These activities constituted four samples as defined by Inspection Procedure 71111.13.
b. Findings
No findings of significance were identified.
1R15 Operability Evaluations
.1 Operability Evaluations
a. Inspection Scope
The inspectors reviewed the following issues:
- 1C steam generator narrow range Level Transducer 1LT-538 out of tolerance;
- centrifugal charging pump shaft failure vulnerability;
- 2B diesel generator electronic governor failure;
- control room ventilation Fire Damper 0VC089Y failed shut;
- 1B diesel generator fuel supply line fretting induced through wall flaw;
- containment spray caustic addition tank mixing time assessment;
- centrifugal charging pump miniflow isolation valves operability during wide range pressure instrument testing and calibration; and
- 2D main steam line pressure rate bistables failure to trip during testing impacting main steam line isolation subsequent to steam line rupture.
8 Enclosure The inspectors selected these potential operability issues based on the risk-significance of the associated components and systems. The inspectors evaluated the technical adequacy of the evaluations to ensure that TS operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the TS and UFSAR to the licensee's evaluations, to determine whether the components or systems were operable. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. The inspectors determined, where appropriate, compliance with bounding limitations associated with the evaluations. Additionally, the inspectors also reviewed a sampling of corrective action documents to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations. Documents reviewed are listed in the Attachment. This inspection constituted eight samples as defined in Inspection Procedure 71111.15.
b. Findings
No findings of significance were identified.
1R18 Plant Modifications
.1 Temporary Plant Modifications
a. Inspection Scope
The inspectors reviewed the following temporary modification:
- 2B reactor vessel level indication system temporary configuration change due to failed plenum area level sensor number four. The inspectors chose to review this temporary modification because it was the longest active modification on site, dating back to January 2005, in addition to its impact on the post accident monitoring system reactor vessel level indication system. The inspectors compared the temporary configuration change and associated 10 CFR 50.59 screening and evaluation information against the design basis, the UFSAR, and the TS, as applicable, to verify that the modification did not affect the operability or availability of the affected system. The inspectors, as applicable, performed field verifications to ensure that the modification was installed as directed; the modification operated as expected; modification testing adequately demonstrated continued system operability, availability, and reliability; and that operation of the modification did not impact the operability of any interfacing systems. Lastly, the inspectors discussed the temporary modification with operations, engineering, and training personnel to ensure that the individuals were aware of how extended operation with the temporary modification in place could impact overall plant performance. Documents reviewed are listed in the Attachment to this report. This inspection constituted one sample as defined in Inspection Procedure 71111.18.
9 Enclosure
b. Findings
No findings of significance were identified.
1R19 Post Maintenance Testing
.1 Post Maintenance Testing
a. Inspection Scope
The inspectors reviewed the following post-maintenance activities to verify that procedures and test activities were adequate to ensure system operability and functional capability:
- 2B residual heat removal pump following an online maintenance window;
- 2A residual heat removal pump following an online maintenance window;
- 1B containment spray train pump and valves following an online maintenance window;
- 2A containment spray train pump and valves following an online maintenance window; and
- Unit 1 instrument inverter 112 following an online maintenance window. These activities were selected based upon the structure, system, or component's ability to impact risk. The inspectors evaluated these activities for the following (as applicable): the effect of testing on the plant had been adequately addressed; testing was adequate for the maintenance performed; acceptance criteria were clear and demonstrated operational readiness; test instrumentation was appropriate; tests were performed as written in accordance with properly reviewed and approved procedures; equipment was returned to its operational status following testing (temporary modifications or jumpers required for test performance were properly removed after test completion), and test documentation was properly evaluated. The inspectors evaluated the activities against TS, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various NRC generic communications to ensure that the equipment met the licensing basis and design requirements. In addition, the inspectors reviewed corrective action documents associated with post-maintenance tests to determine whether the licensee was identifying problems and entering them in the corrective action program and that the problems were being corrected commensurate with their importance to safety. Documents reviewed are listed in the Attachment. This inspection constituted five samples as defined in Inspection Procedure 71111.19.
b. Findings
No findings of significance were identified 10 Enclosure
1R22 Surveillance Testing
.1 Routine Surveillance Testing
a. Inspection Scope
The inspectors reviewed the test results for the following activities to determine whether risk-significant systems and equipment were capable of performing their intended safety function and to verify testing was conducted in accordance with applicable procedural and TS requirements:
- 1B solid state protection system bi-monthly operability test;
- 1B diesel generator semi-annual engineered safeguards feature start and monthly run; and
- review of licensee's procedure for auxiliary building ventilation non-accessible area exhaust filter plenum performance in emergency mode regarding frequency and methodology for ensuring emergency core cooling system rooms are maintained at a greater vacuum than general plant areas. The inspectors observed in-plant activities and reviewed procedures and associated records to determine whether: any preconditioning occurred; effects of the testing were adequately addressed by control room personnel or engineers prior to the commencement of the testing; acceptance criteria were clearly stated, demonstrated operational readiness, and were consistent with the system design basis; plant equipment calibration was correct, accurate, and properly documented; as left setpoints were within required ranges; the calibration frequency was in accordance with TS, the UFSAR, procedures, and applicable commitments; measuring and test equipment calibration was current; test equipment was used within the required range and accuracy; applicable prerequisites described in the test procedures were satisfied; test frequencies met TS requirements to demonstrate operability and reliability; tests were performed in accordance with the test procedures and other applicable procedures; jumpers and lifted leads were controlled and restored where used; test data and results were accurate, complete, within limits, and valid; test equipment was removed after testing; where applicable, test results not meeting acceptance criteria were addressed with an adequate operability evaluation or the system or component was declared inoperable; where applicable for safety-related instrument control surveillance tests, reference setting data were accurately incorporated in the test procedure; where applicable, actual conditions encountering high resistance electrical contacts were such that the intended safety function could still be accomplished; prior procedure changes had not provided an opportunity to identify problems encountered during the performance of the surveillance or calibration test; equipment was returned to a position or status required to support the performance of the safety functions; and all problems identified during the testing were appropriately documented and dispositioned in the corrective action program. Documents reviewed are listed in the Attachment. This inspection constituted three routine surveillance testing samples as defined in Inspection Procedure 71111.22.
11 Enclosure
b. Findings
Introduction:
The inspectors identified a Green non-cited violation (NCV) for the failure to comply with 10 CFR 50, Appendix B, Criteria V, Instructions, Procedures, and Drawings when the licensee failed to establish adequate acceptance criteria for performing a surveillance required by the plant's TSs.
Description:
During a review of the licensee's process for restoring a room containing emergency core cooling system (ECCS) components to service when a plant barrier impairment (PBI) has been used to support on-line maintenance, the inspectors noted an issue with the adequacy of the acceptance criteria for TS Surveillance Requirement 3.7.12.4 Auxiliary Building Non-Accessible System Filter Plenum Test. Specifically, the acceptance criteria did not include a verification of air flow from the general areas of the auxiliary building to the ECCS rooms. The design basis of the non-accessible area exhaust filter plenum ventilation system is to limit radioactive release to within the 10 CFR 50.67 accident source term limits in the event of a large break loss of coolant accident (LOCA) with an assumed passive failure in the ECCS outside containment such as a pump seal failure. The control room habitability analysis also credits the functionality of the non-accessible area exhaust filter plenum ventilation system. Technical Specification 3.7.12 ensures the operability of the non-accessible area ventilation system and was described in the bases section as ensuring air flow from areas of low potential contamination to areas of high potential contamination by maintaining spaces which have the potential to contain highly radioactive fluids during the recirculation phase of post LOCA ECCS operation at a negative pressure with respect to adjacent spaces. Surveillance Requirement 3.7.12.4 required that the non-accessible area exhaust filter plenum ventilation system maintain a pressure differential of -0.25 inches water column between the spaces served by the system and atmospheric pressure. The licensee procedure accomplishing this requirement measured the differential pressures between the atmosphere and turbine building, the turbine building and the auxiliary building, and the auxiliary building and the potentially contaminated spaces served by the non-accessible plenum ventilation system. These differentials were summed to ensure -0.25 inches water column was achieved. The normal auxiliary building ventilation lineup maintains a < -0.5 inches water column differential pressure between the turbine building and the auxiliary building. This large negative differential itself could quantitatively ensure that the Technical Specification acceptance criteria is met without meeting the design basis intent of the system to ensure that airflow was from areas of low potential contamination (general areas of the auxiliary building) to areas of high potential contamination post LOCA (ECCS rooms).
Analysis:
The inspectors determined that failing to establish an acceptance criteria ensuring the design basis function of the non-accessible area exhaust filter plenum ventilation system was met was a performance deficiency warranting a significance evaluation in accordance with Inspection Manual Chapter (IMC) 0612, "Power Reactor Inspection Reports," Appendix B, "Issue Screening," dated September 20, 2007. This finding is greater than minor because it is associated with the attribute for maintaining the radiological barrier functionality of the control room and auxiliary building by the use of quality procedures, and affected the barrier integrity cornerstone objective of providing reasonable assurance that physical design barriers protect the public from radionuclide 12 Enclosure releases caused by accidents or events. This finding was reviewed using IMC 0609, "Significance Determination Process, Attachment 0609.04, "Phase 1 - Initial Screening and Characterization of Finding," dated January 10, 2008. The finding was determined to be of very low safety significance because the inspector answered no to all the questions for the significance screening associated with the Barrier's Cornerstone. Furthermore, a review of past surveillance testing verified no actual system inoperability has existed, and the failure to establish a formal acceptance criteria for air flow only impacted non-accessible area exhaust filter plenum ventilation system.
Enforcement:
10 CFR 50, Appendix B, Criteria V, Instructions, Procedures, and Drawings states in part, instructions, procedures, or drawings shall include appropriate quantitative or qualitative acceptance criteria for determining that important activities have been satisfactorily accomplished. Contrary to the above, the licensee failed to establish acceptance criteria verifying the direction of air flow in the auxiliary building during operation in the emergency mode of the non-accessible exhaust filter plenum ventilation system. Because this failure to comply with 10 CFR 50, Appendix B, Criterion V, is of very low safety significance and has been entered into the licensee's corrective action program, as Issue Report 723736, this violation is being treated as an NCV, consistent with Section VI.A of the NRC Enforcement Policy: (NCV 05000456/2008002-01, 05000457/2008002-01 Inadequate Acceptance Criteria Established in TS Surveillance Requirement.)
.2 Inservice Testing Surveillance
a. Inspection Scope
The inspectors reviewed the test results for the following activities to determine whether risk-significant systems and equipment were capable of performing their intended safety function and to verify testing was conducted in accordance with applicable procedural and TS requirements:
- 2A centrifugal charging pump quarterly American Society of Mechanical Engineers (ASME) test; and
- 1B safety injection pump quarterly ASME test. The inspectors observed in-plant activities and reviewed procedures and associated records to determine whether: any preconditioning occurred; effects of the testing were adequately addressed by control room personnel or engineers prior to the commencement of the testing; acceptance criteria were clearly stated, demonstrated operational readiness, and were consistent with the system design basis; plant equipment calibration was correct, accurate, and properly documented; as left setpoints were within required ranges; and the calibration frequency were in accordance with TSs, the UFSAR, procedures, and applicable commitments; measuring and test equipment calibration was current; test equipment was used within the required range and accuracy; applicable prerequisites described in the test procedures were satisfied; test frequencies met TS requirements to demonstrate operability and reliability; tests were performed in accordance with the test procedures and other applicable procedures; jumpers and lifted leads were controlled and restored where used; test data and results were accurate, complete, within limits, and valid; test equipment was removed after testing; where applicable for inservice testing activities, testing was performed in accordance with the applicable version of Section XI, ASME Code, and reference values 13 Enclosure were consistent with the system design basis; where applicable, test results not meeting acceptance criteria were addressed with an adequate operability evaluation or the system or component was declared inoperable; where applicable for safety-related instrument control surveillance tests, reference setting data were accurately incorporated in the test procedure; where applicable, actual conditions encountering high resistance electrical contacts were such that the intended safety function could still be accomplished; prior procedure changes had not provided an opportunity to identify problems encountered during the performance of the surveillance or calibration test; equipment was returned to a position or status required to support the performance of its safety functions; and all problems identified during the testing were appropriately documented and dispositioned in the corrective action program. Documents reviewed are listed in the Attachment. This inspection constituted two inservice inspection samples as defined in Inspection Procedure 71111.22.
b. Findings
No findings of significance were identified.
.3 Reactor Coolant System Leak Detection Inspection Surveillance
The inspectors reviewed the test results for the following activities to determine whether risk-significant systems and equipment were capable of performing their intended safety function and to verify testing was conducted in accordance with applicable procedural and TS requirements:
- Unit 1 reactor coolant system water inventory balance surveillance. The inspectors observed in plant activities and reviewed procedures and associated records to determine whether: preconditioning occurred; effects of the testing were adequately addressed by control room personnel or engineers prior to the commencement of the testing; acceptance criteria were clearly stated, demonstrated operational readiness, and were consistent with the system design basis; plant equipment calibration was correct, accurate, and properly documented; as left setpoints were within required ranges; and the calibration frequency were in accordance with TSs, the UFSAR, procedures, and applicable commitments; measuring and test equipment calibration was current; test equipment was used within the required range and accuracy; applicable prerequisites described in the test procedures were satisfied; test frequencies met TS requirements to demonstrate operability and reliability; tests were performed in accordance with the test procedures and other applicable procedures; jumpers and lifted leads were controlled and restored where used; test data and results were accurate, complete, within limits, and valid; test equipment was removed after testing; where applicable, test results not meeting acceptance criteria were addressed with an adequate operability evaluation or the system or component was declared inoperable; where applicable for safety-related instrument control surveillance tests, reference setting data were accurately incorporated in the test procedure; where applicable, actual conditions encountering high resistance electrical contacts were such that the intended safety function could still be accomplished; prior procedure changes had not provided an opportunity to identify problems encountered during the performance of the surveillance or calibration test; equipment was returned to a position 14 Enclosure or status required to support the performance of its safety functions; and all problems identified during the testing were appropriately documented and dispositioned in the corrective action program. Documents reviewed are listed in the Attachment. This inspection constituted one reactor coolant system leak detection inspection sample as defined in Inspection Procedure 71111.22.
b. Findings
No findings of significance were identified.
===Cornerstone: Emergency Preparedness [EP]
1EP6 Drill Evaluation
.1 Emergency Preparedness Drill Observation
=
a. Inspection Scope
The inspectors evaluated the conduct of a routine licensee emergency drill on February 13, 2008, to identify any weaknesses and deficiencies in classification, notification, and protective action recommendation development activities. The inspectors observed emergency response operations in the Technical Support Center and the Operational Support Center to determine whether the event classification, notifications, and protective action recommendations were performed in accordance with procedures. The inspectors also attended the licensee drill critique to compare any inspector-observed weakness with those identified by the licensee staff in order to evaluate the critique and to verify whether the licensee staff was properly identifying weaknesses and entering them into the corrective action program. As part of the inspection, the inspectors reviewed the drill package and other documents listed in the Attachment. This inspection constituted one sample as defined in Inspection Procedure 71114.06.
b. Findings
No findings of significance were identified.
RADIATION SAFETY
===Cornerstone: Occupational Radiation Safety 2OS3 Radiation Monitoring Instrumentation and Protective Equipment (71121.03)
.1 Inspection Planning
=
a. Inspection Scope
The inspectors reviewed the plant UFSAR to identify applicable radiation monitors associated with transient high and very high radiation areas, including those used in remote emergency assessment.
15 Enclosure This inspection constituted one sample as defined by Inspection Procedure 71121.03. The inspectors identified the types of portable radiation detection instrumentation used for job coverage of high radiation area work, other temporary area radiation monitors currently used in the plant, continuous air monitors associated with jobs with the potential for workers to receive 50 mrem committed effective dose equivalent (CEDE), whole body counters, and the types of radiation detection instruments utilized for personnel release from the radiologically controlled area.
This inspection constitutes one sample as defined by Inspection Procedure 71121.03. The inspectors verified calibration, operability, and alarm setpoint (if applicable) of the following instruments:
- FastScan Wholebody Counter;
- Eberline RO-20;
- Eberline PM-7; and
- IPM 7 Wholebody Frisking Machine. The inspectors determined what actions were taken when, during calibration or source checks, an instrument was found significantly out of calibration (greater than 50 percent), determined possible consequences of instrument use since last successful calibration or source check, and determined if the out of calibration result was entered into the corrective action program. There were no instances where the instruments were found significantly out of calibration. The inspectors also reviewed the licensee's 10 CFR Part 61 source term reviews to determine if the calibration sources used were representative of the plant source term. This inspection constituted one sample as defined by Inspection Procedure 71121.03.
Documents reviewed are listed in the Attachment to this report.
b. Findings
No findings of significance were identified.
.2 Problem Identification and Resolution
a. Inspection Scope
The inspectors reviewed the licensee's self-assessments, audits, Licensee Event Reports, and Special Reports that involved personnel contamination monitor alarms due to personnel internal exposures to verify that identified problems were entered into the corrective action program for resolution. All event reports involving internal exposures >50 mrem CEDE were reviewed to determine if the affected personnel were properly monitored utilizing calibrated equipment and if the data was analyzed and internal exposures properly assessed in accordance with licensee procedures. This inspection constituted one sample as defined by Inspection Procedure 71121.03.
16 Enclosure The inspectors reviewed corrective action program reports related to exposure significant radiological incidents that involved radiation monitoring instrument deficiencies since the last inspection in this area. Staff members were interviewed and corrective action documents were reviewed to verify that follow-up activities were being conducted in an effective and timely manner commensurate with their importance to safety and risk based on the following:
- Initial problem identification, characterization, and tracking;
- Disposition of operability/reportability issues;
- Evaluation of safety significance/risk and priority for resolution;
- Identification of repetitive problems;
- Identification of contributing causes;
- Identification and implementation of effective corrective actions;
- Resolution of NCVs tracked in the corrective action system; and
- Implementation/consideration of risk significant operational experience feedback. This inspection constituted one sample as defined by Inspection Procedure 71121.03. The inspectors determined if the licensee's self-assessment activities were identifying and addressing repetitive deficiencies or significant individual deficiencies in problem identification and resolution.
This inspection constituted one sample as defined by Inspection Procedure 71121.03. Documents reviewed are listed in the Attachment to this report.
b. Findings
No findings of significance were identified.
.3 Radiation Protection Technician Instrument Use
a. Inspection Scope
The inspectors verified the calibration expiration and source response check currency on radiation detection instruments staged for use and observed radiation protection technicians for appropriate instrument selection and self-verification of instrument operability prior to use. Documents reviewed are listed in the Attachment to this report. This inspection constituted one sample as defined by Inspection Procedure 71121.03.
b. Findings
No findings of significance were identified.
.4 Self-Contained Breathing Apparatus (SCBA) Maintenance and User Training
a. Inspection Scope
The inspectors reviewed the status and surveillance records of SCBAs staged and ready for use in the plant and inspected the licensee's capability for refilling and transporting SCBA air bottles to and from the control room and operations support center during 17 Enclosure emergency conditions. The inspectors observed an unannounced fire drill that included donning staged SCBAs, and the inspectors assessed the licensee's response to SCBA bottle failures identified during that drill. The inspectors determined if control room operators and other emergency response and radiation protection personnel were trained and qualified in the use of SCBAs (including personal bottle change-out). The inspectors verified the training and qualification status of individuals on each control room shift crew and three individuals from each designated department were currently assigned emergency duties (e.g., onsite search and rescue duties). This inspection constituted one sample as defined by Inspection Procedure 71121.03. The inspectors reviewed the qualification documentation for personnel designated to perform maintenance on the vendor-designated vital components, and the vital component maintenance records over the past five years for three SCBA units currently designated as "ready for service." No on-site personnel were assigned to repair vital components. All vital component repair was conducted by manufacturer representatives. The inspectors also ensured that the required, periodic air cylinder hydrostatic testing was documented and up to date, and that the Department of Transportation required retest air cylinder markings were in place for these three units. The inspectors reviewed the onsite maintenance procedures governing vital component work, including those for the low-pressure alarm and pressure-demand air regulator; licensee procedures; and the SCBA manufacturer's recommended practices to determine if there were inconsistencies between them. This inspection constituted one sample as defined by Inspection Procedure 71121.03. Documents reviewed are listed in the Attachment to this report.
b. Findings
No findings of significance were identified. Cornerstone: Public Radiation Safety 2PS1 Radioactive Gaseous and Liquid Effluent Treatment and Monitoring Systems (71122.01) Review of Blowdown Line Operations and Tritium Remediation Efforts The inspectors continued to monitor the licensee's activities resulting from previous inadvertent leaks of tritiated liquid from the blowdown line to the Kankakee River. The inspection activities included the following:
- periodic inspections of all vacuum breaker vaults;
- periodic inspections of remediation system pump operations at the Exelon Pond, vacuum breaker 1, vacuum breaker 2, and lagoon area;
- efforts to reduce tritium concentrations in secondary plant systems; and
- participation in Community Information Meetings. The inspectors verified that minor issues identified during these inspection activities were entered into the licensee's corrective action program. This inspection did not 18 Enclosure represent a completed inspection sample. Documents reviewed are listed in the Attachment to this report.
b. Findings
No findings of significance were identified.
OTHER ACTIVITIES
4OA1 Performance Indicator Verification
.1 Data Submission Issue
a. Inspection Scope
The inspectors performed a review of the data submitted by the licensee for the First Quarter 2008 performance indicators for any obvious inconsistencies prior to its public release in accordance with IMC 0608, "Performance Indicator Program." This review was performed as part of the inspectors' normal plant status activities and, as such, did not constitute a separate inspection sample.
b. Findings
No findings of significance were identified.
.2 Unplanned Scrams per 7000 Critical Hours
a. Inspection Scope
The inspectors sampled licensee submittals for the Unplanned Scrams per 7000 Critical Hours performance indicator for Unit 1 and Unit 2 for the period from First Quarter 2007 through Fourth Quarter 2007. To determine the accuracy of the Performance Indicator (PI) data reported during those periods, PI definitions and guidance contained in Revision 5 of the Nuclear Energy Institute (NEI) Document 99-02, "Regulatory Assessment Performance Indicator Guideline," were used. The inspectors reviewed the licensee's operator narrative logs, issue reports, event reports and NRC Inspection reports for the period of January 2007 through December 2007 to validate the accuracy of the submittals. The inspectors also reviewed the licensee's issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified. Specific documents reviewed are described in the Attachment. This inspection constituted two unplanned scrams per 7000 critical hours samples as defined by Inspection Procedure 71151.
b. Findings
No findings of significance were identified.
19 Enclosure
.3 Unplanned Scrams with Complications
a. Inspection Scope
The inspectors sampled licensee submittals for the Unplanned Scrams with Complications performance indicator for Unit 1 and Unit 2 for the period from the First Quarter 2007 through Fourth Quarter 2007. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in Revision 5 of NEI Document 99-02, "Regulatory Assessment Performance Indicator Guideline," were used. The inspectors reviewed the licensee's operator narrative logs, issue reports, event reports and NRC Integrated Inspection reports for the period of January 2007 through December 2007, to validate the accuracy of the submittals. The inspectors also reviewed the licensee's issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified. Specific documents reviewed are described in the Attachment. This inspection constituted two unplanned scrams with complications samples as defined by Inspection Procedure 71151.
b. Findings
No findings of significance were identified.
.4 Unplanned Transients per 7000 Critical Hours
a. Inspection Scope
The inspectors sampled licensee submittals for the Unplanned Transients per 7000 Critical Hours performance indicator for Unit 1 and Unit 2 for the period from the First Quarter 2007 through Fourth Quarter 2007. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in Revision 5 of the NEI Document 99-02, "Regulatory Assessment Performance Indicator Guideline," were used. The inspectors reviewed the licensee's operator narrative logs, issue reports, maintenance rule records, event reports and NRC Integrated Inspection reports for the period of January 2007 through December 2007, to validate the accuracy of the submittals. The inspectors also reviewed the licensee's issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified. Specific documents reviewed are described in the Attachment. This inspection constituted two unplanned transients per 7000 critical hours samples as defined by Inspection Procedure 71151.
b. Findings
No findings of significance were identified.
20 Enclosure
4OA2 Identification and Resolution of Problems
.1 Routine Review of items Entered Into the Corrective Action Program
a. Scope
As part of the various baseline inspection procedures discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that they were being entered into the licensee's CAP at an appropriate threshold, that adequate attention was being given to timely corrective actions, and that adverse trends were identified and addressed. Attributes reviewed included: the complete and accurate identification of the problem; that timeliness was commensurate with the safety significance; that evaluation and disposition of performance issues, generic implications, common causes, contributing factors, root causes, extent of condition reviews, and previous occurrences reviews were proper and adequate; and that the classification, prioritization, focus, and timeliness of corrective actions were commensurate with safety and sufficient to prevent recurrence of the issue. Minor issues entered into the licensee's CAP as a result of the inspectors' observations are included in the attached list of documents reviewed. Routine reviews for the identification and resolution of problems were not considered additional inspection samples. Instead, by procedure they were considered an integral part of the inspections performed during the quarter and documented in Section 1 of this report.
b. Findings
No findings of significance were identified.
.2 Daily Corrective Action Program Reviews
a. Scope
In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the licensee's CAP. This review was accomplished through inspection of the station's daily condition report packages. These daily reviews were performed by procedure as part of the inspectors' daily plant status monitoring activities and, as such, did not constitute any separate inspection samples.
b. Findings
No findings of significance were identified.
21 Enclosure
.3 Selected Issue Follow-up Inspection: Underground piping corrosion control program review
a. Scope
The inspectors reviewed the licensee's program for mitigating corrosion in buried piping and raw water systems. The licensee has experienced through wall leakage in two lengths of moderate energy ASME Class III essential service water piping, a failure of an underground feed pipe to the Unit 2 auxiliary boiler resulting in tritiated water spilling into the groundwater on site, and underground piping leaks in the potable water system over the past year. In response to these and other fleet wide issues, the licensee was in the process of establishing a database identifying the location, construction, and susceptibility of the site's underground and raw water system piping. This database was intended to incorporate a matrixing system to include a number of variables that impact both internal and externally induced corrosion and ensure that the most susceptible piping was inspected at intervals that precludes piping leaks and failures. Previous licensee corrosion control methodology was based on internal corrosion criteria such as the type of fluid in the pipe, regularity and intensity of flow in the pipe, and the chemistry of the fluid in the pipe. The new program adds inputs for the piping material, presence of groundwater, and other external corrosion concerns. The inspectors reviewed the Dresden database that was near completion. Braidwood expected to have a working database by the end of calendar year 2008. In addition the inspectors reviewed the material condition of the site's cathodic protection system.
The licensee was working to overcome specific challenges that piping used during original construction was not well documented in plant drawings. Most significantly, the water table was very close to the surface over much of the site. This made excavation extremely difficult and expensive (creating a need for cofferdams), made searching for underground piping using existing non-destructive technologies more difficult and significantly added to the likelihood of underground piping corrosion. The licensee's creation of a scientific database for classifying piping based on corrosion susceptibility and risk (radiological, nuclear safety) was determined to aid plant engineering's created inspection frequency criteria with the potential to minimize leaks and failures. The main challenge remained reaching and inspecting susceptible piping on a regular basis.
The above constituted completion of one in-depth problem identification and resolution sample.
b. Findings
No findings of significance were identified.
.4 Selected Issue Follow-up Inspection: Reactor Coolant System Perturbation While Venting the 2B Reactor Coolant Pump Seal Injection Filter
Annual Sample: Human Performance Induced Plant Transients
a. Inspection Scope
The inspectors reviewed equipment and plant transients over the previous year to determine if human performance may have been a contributing factor. Specifically, the 22 Enclosure inspectors reviewed the licensee's response to a minor plant transient induced by excessive venting of the 2B reactor coolant pump (RCP) seal injection filter following replacement. The inspectors reviewed the corrective action program to determine if any trends existed in the area of RCP seal injection filter venting, or other human performance issues, and plant transients.
The inspectors interviewed plant operations personnel, reviewed corrective action documents, and reviewed the licensee's actions to address a minor transient caused by excessive RCP seal injection filter venting on the night shift of February 10, 2008. The excessive venting resulted in a 2 percent drop in pressurizer level, an increase in the RCS charging rate, and a drop in seal injection flow to all four RCPs. The licensee's initial response was not adequate in that the initial corrective action document and control room log entry were not sufficient in describing the plant response to the excessive filter venting, the oncoming day shift manager was unaware of the issue following turnover, and a site-wide human performance safety stand down on February 12 did not include this issue among the human performance examples.
Subsequently, based on questioning by the inspectors and members of the licensee's organization, an additional corrective action document of adequate detail was generated and a quick human performance investigation was initiated. The inspectors determined the licensee's actions were ultimately appropriate; however these actions were unnecessarily delayed. The inspectors' review of other plant transients in the past year did not identify a trend in human performance induced transients.
b. Findings
No findings of significance were identified
4OA3 Follow-up of Events and Notices of Enforcement Discretion
.1 Unit 1 Shutdown Bank "B" Control Rod J13 Dropped Into Core From Steady State Conditions
a. Inspection Scope
The inspectors reviewed the plant's response to a dropped Control Rod (J13) during steady state plant operations on Unit 1. On January 8, 2008, Shutdown Bank Control Rod J13 dropped into the core. No control rod demand signals were present and no other significant plant evolutions were in progress at the time of the event. Plant operators immediately entered the site's off-normal procedure for misaligned control rods and began to ramp the unit down to 1200 MWe to maintain plant parameters in band. After further investigation did not reveal an immediately identifiable cause for the dropped control rod, reactor power was further reduced to 70 percent (880 MWe) in accordance with the off-normal procedure. The licensee established a troubleshooting team which included off-site vendor and corporate support. Further advanced troubleshooting did not identify an existing faulted condition in the rod control system.
Troubleshooting did identify a stationary control rod drive mechanism (CRDM) gripper current of 3.9 amps for Rod J13, which was slightly lower than the expected value of just over 4 amps. Vendor testing indicated that control rods can be held with gripper currents as low as 3.0 amps. In response to the low gripper current, the licensee installed a temporary modification including a regulation card which boosts stationary 23 Enclosure gripper current approximately 10 percent for all shutdown bank B control rods. The inspectors observed licensee troubleshooting and management decision making meetings. In addition, the inspectors observed the installation of the temporary modification and monitoring equipment to capture data in the event a subsequent perturbation in the rod control system were to occur. With the temporary modification and electronic monitoring equipment installed and no remaining faulted condition in the Unit 1 rod control system present, the licensee reduced power to 39 percent and recovered the control rod. The inspectors attended the pre-evolution brief and observed the operators perform the recovery. The licensee's root cause report identified an intermittent open most likely tied to a loose pin connection in the stationary gripper control circuit as the most probable cause of the dropped rod.
Continued investigation for a possible defective pin and meggar testing of the CRDM for Rod J13 was scheduled for the next refueling outage A1R14. Documents reviewed in this inspection are listed in the Attachment.
This inspection constituted one sample as defined in Inspection Procedure 71153.
b. Findings
No findings of significance were identified.
.2 Loss of the 2B Main Feedwater Pump and Operator Induced Turbine Runback
a. Inspection Scope
On the morning of February 14, 2008, with the 2C feedwater pump out-of-service for a maintenance work window, operators in the control room received indications of lowering electro-hydraulic (EH) fluid sump level. Field operators were dispatched and reported a leak on the EH piping to the 2B feedwater pump. As a result, control room operators began ramping down Unit 2 at 50 MWe/min. Operators noticed the 2B feedwater pump speed decreasing during the ramp down. Due to the decreasing pump speed, operators initiated a turbine runback and manually tripped the 2B feedwater pump. The licensee isolated the EH fluid leak and stabilized the plant at approximately 55 percent power. The motor driven feedwater pump continued to operate normally providing feedwater to the steam generators. The inspectors reviewed the operators' response to this event as well as the repairs to the electro-hydraulic control system and eventual plant recovery. The inspectors determined that the licensee's actions during and after this event were reasonable and did not constitute a performance deficiency. Documents reviewed as a part of this inspection are listed in the Attachment. This inspection constituted one sample as defined in Inspection Procedure 71153.
b. Findings
No findings of significance were identified.
24 Enclosure
.3 (Closed) Licensee Event Report (LER) 05000456/2007-003-00:
Improper Installation of Insulation on the Unit 1 Main Steam Safety Valves This event, which occurred on October 24, 2007, was previously reported in Inspection Report 05000456/2007006; 05000457/2007006, Section 1R15. On October 24, 2007, with the unit in Mode 3 (shutdown with reactor coolant temperature > 350
°F) and exiting a refueling outage, a licensee maintenance supervisor noted that a total of 10 main steam safety valves associated with the A and D steam generators were fully insulated. These valves had never been insulated since initial construction. Licensee system engineering had insulation installed on the safety valves due to the high temperatures experienced in the safety valve room shared by the A and D steam generators in order to protect other equipment in the space from over temperature conditions. The supervisor wrote an issue report asking for an assessment to be made on how the insulation could possibly affect the lift characteristics of the valves. The inspectors noted this issue report during their daily issue report review and immediately spoke with licensee design engineering. Licensee engineering engaged the vendor and determined that the presence of insulation on the valve body caused the valve to experience higher temperatures and impact the valve's lift spring causing the lift setpoint to be reduced outside of the TS acceptance band. On October 26, 2008, the insulation was removed from all ten valves with the plant in Mode 1 (reactor power > 5 percent). Operating with four or more safety valves inoperable for more than 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> in Modes 1, 2 or 3 is not permitted by TS 3.7.1. The licensee performed Trevi testing on three of the safety valves impacted by the insulation on December 9, 2007, to ensure that there were no lasting effects on the lift setpoints of the valves that had been insulated. All three valves lifted within the +/-3 percent tolerance permitted by the TS. In addition, the licensee tested a spare safety valve offsite mimicking the conditions experienced by the installed safety valves when insulated to validate the impact insulating the valve body had on the valve internals. Four lifts of the spare valve were performed with all falling below the acceptable range, therefore validating the assumption by the licensee and the vendor that the valves were inoperable during the time period they were insulated. This licensee-identified finding involved a violation of TS 3.7.1. The enforcement aspects of this violation are discussed in Section 4OA7. Documents reviewed as a part of this inspection are listed in the Attachment. This LER is closed. This inspection constituted one sample as defined in Inspection Procedure 71153.
4OA5 Other Activities
.1 Quarterly Resident Inspector Observations of Security Personnel and Activities
a. Inspection Scope
During the inspection period, the inspectors conducted the following observations of security force personnel and activities to ensure that the activities were consistent with licensee security procedures and regulatory requirements relating to nuclear plant security. These observations took place during both normal and off-normal plant working hours.
- Multiple tours of operations within the security alarm stations;
- Tours of selected security officer response posts;
- Direct observation of personnel entry screening operations within the plant's Main Access Facility; and
- Security force shift turnover activities. These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples. Rather, they were considered an integral part of the inspectors' normal plant status review and inspection activities.
b. Findings
No findings of significance were identified.
4OA6 Management Meetings
.2 Exit Meeting Summary
On April 10, 2008, the inspectors presented the inspection results to Mr. B. Hanson, and other members of the licensee staff. The licensee acknowledged the issues presented. The inspector asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.
.3 Interim Exit Meetings
Radiation monitoring instrumentation and protective equipment with Mr. L. Coyle, Plant Manager and his staff on March 14, 2008.
The licensee acknowledged the issues presented. The inspector asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.
4OA7 Licensee-Identified Violations
The following violation of very low significance (Green) was identified by the licensee and is a violation of NRC requirements which meets the criteria of Section VI of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as an NCV.
- Technical Specification 3.7.1 required that the plant be in Mode 4 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> when any one steam generator had four or more main steam safety inoperable. Contrary to this, between October 24, 2007 and October 26, 2007, both the A and D steam generators operated in Modes 1, 2, and 3 with 5 inoperable main steam safety valves each. This was identified in the licensee's corrective action program as Issue Report 689141. This finding was of very low safety significance because it did not represent a loss of secondary plant heat removal capability or secondary plant depressurization capability. ATTACHMENT:
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee
- B. Hanson, Site Vice President
- L. Coyle, Plant Manager
- S. Butler, Emergency Preparedness Manager
- G. Dudek, Site Training Director
- R. Gadbois, Maintenance Director
- D. Gullott, Regulatory Assurance Manager
- H. Hanoun, Acting Chemistry, Environmental, and Radioactive Waste Manager
- J. Knight, Nuclear Oversight Manager
- T. McCool, Operations Director
- J. Moser, Radiation Protection Manager
- J. Petty, Licensing Engineer
- M. Smith, Engineering Director Nuclear Regulatory Commission
- R. Skokowski, Chief, Reactor Projects Branch 3
LIST OF ITEMS
OPENED, CLOSED AND DISCUSSED
Opened and Closed
- 05000457/2008002-01 NCV Inadequate Acceptance Criteria Established in Technical Specification Surveillance Requirement (Section 1R22)
Closed
- 05000456/2007-003-00 LER Improper Installation of Insulation on the Unit 1 Main Steam Safety Valves (Section 4OA3.3)
Attachment
LIST OF DOCUMENTS REVIEWED
The following is a partial list of documents reviewed during the inspection.
- Inclusion on this list does not imply that the NRC inspector reviewed the documents in their entirety, but rather that selected sections or portions of the documents were evaluated as part of the overall inspection effort.
- Inclusion of a document on this list does not imply NRC acceptance of the document or any part of it, unless this is stated in the body of the inspection report.