IR 05000390/2013007: Difference between revisions

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| issue date = 04/08/2013
| issue date = 04/08/2013
| title = IR 05000390-13-007, 02/04-8/2013 and 02/19-22/2013, Watts Bar Nuclear Plant, Unit 1, Biennial Inspection of the Identification and Resolution of Problems
| title = IR 05000390-13-007, 02/04-8/2013 and 02/19-22/2013, Watts Bar Nuclear Plant, Unit 1, Biennial Inspection of the Identification and Resolution of Problems
| author name = Hopper G T
| author name = Hopper G
| author affiliation = NRC/RGN-II/DRP/RPB7
| author affiliation = NRC/RGN-II/DRP/RPB7
| addressee name = Shea J W
| addressee name = Shea J
| addressee affiliation = Tennessee Valley Authority
| addressee affiliation = Tennessee Valley Authority
| docket = 05000390
| docket = 05000390
Line 18: Line 18:


=Text=
=Text=
{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION REGION II 245 PEACHTREE CENTER AVENUE NE, SUITE 1200 ATLANTA, GEORGIA 30303-1257 April 8, 2013 Mr. Joseph Vice President Nuclear Licensing Tennessee Valley Authority 1101 Market Street, LP 3D-C
{{#Wiki_filter:April 8, 2013


Chattanooga, TN 37402-2801 SUBJECT: WATTS BAR NUCLEAR PLANT, UN IT 1 - NRC PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000390/2013007
==SUBJECT:==
WATTS BAR NUCLEAR PLANT, UN IT 1 - NRC PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000390/2013007


==Dear Mr. Shea:==
==Dear Mr. Shea:==
Line 33: Line 34:
One NRC identified finding of very low safety significance (Green) was identified during this inspection. The finding did not involve a violation of NRC requirements. If you disagree with the crosscutting aspect assigned to the finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement to the  
One NRC identified finding of very low safety significance (Green) was identified during this inspection. The finding did not involve a violation of NRC requirements. If you disagree with the crosscutting aspect assigned to the finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement to the  


Regional Administrator, RII, and the NRC Senior Res ident Inspector at the Watts Bar Nuclear Plant, Unit 1. In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electr onically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRC's document system (ADAMS). Adams is accessible from the NRC Web site at http://www.nrc.gov/reading- rm/adams.html (the Public Electronic Reading Room).
Regional Administrator, RII, and the NRC Senior Res ident Inspector at the Watts Bar Nuclear Plant, Unit 1. In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electr onically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRC's document system (ADAMS). Adams is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).


Sincerely,
Sincerely,
Line 41: Line 42:
Docket No.: 50-390 License No.: NPF-90  
Docket No.: 50-390 License No.: NPF-90  


Enclosure: Inspection Report 05000390/2013007 w/Attachment: Supplemental Information  
===Enclosure:===
Inspection Report 05000390/2013007 w/Attachment: Supplemental Information  


cc w/encl.: (see page 3)
REGION II==
 
__ _____ X SUNSI REVIEW COMPLETE OFFICE RII:DRP RII:DRP RII:DRP RII:DRP RII:DRS RII:DRP SIGNATURE /RA/ /RA By E-mail/ /RA/ /RA By JHamman for///R By E-mail/ /RA By E-mail/ NAME NStaples TVukovinsky GHopper SSchaefer RWilliams SNinh DATE 3/26/2013 3/18/2013 4/8/2013 4/4/2013 3/19/2013 3/18/2013 E-MAIL COPY? YES NO YES NO YES N YES NO YES N YES NO YES NO cc w/encl:
D. E. Grissette Vice President Watts Bar Nuclear Plant, ADM 1V-WBN Tennessee Valley Authority Electronic Mail Distribution
 
G. A. Boerschig Plant Manager Watts Bar Nuclear Plant, MOB 2R-WBN Tennessee Valley Authority Electronic Mail Distribution
 
C. J. Riedl Acting Manager, Licensing Watts Bar Nuclear Plant, ADM 1L-WBN Tennessee Valley Authority P.O. Box 2000 Spring City, TN 37381
 
J. Manager, Corp. Nuclear Licensing - WBN Tennessee Valley Authority Electronic Mail Distribution E. J. Vigluicci Assistant General Counsel Tennessee Valley Authority Electronic Mail Distribution W. D. Crouch Licensing Manager, Unit 2 Watts Bar Nuclear Plant, EQB 1B-WBN Tennessee Valley Authority P.O. Box 2000
 
Spring City, TN 37381
 
County Mayor P.O. Box 156
 
Decatur, TN 37322
 
County Executive 375 Church Street Suite 215 Dayton, TN 37321
 
Tennessee Department of Enviornment &
Conservation Division of Radiological Health
 
401 Church Street
 
Nashville, TN
 
37243 Senior Resident Inspector U.S. Nuclear Regulatory Commission Watts Bar Nuclear Plant 1260 Nuclear Plant Road
 
Spring City, TN 37381-2000 Ann Harris
 
341 Swing Loop
 
Rockwood, TN 37854 Letter to Joseph from George T. Hopper dated April 8, 2013.
 
SUBJECT: WATTS BAR NUCLEAR PLANT, UN IT 1 - NRC PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000390/2013007
 
Distribution w/encl
: C. Evans, RII L. Douglas, RII OE Mail RIDSNRRDIRS PUBLIC RidsNrrPMWattsBar1 Resource RidsNrrPMWattsBar2 Resource U.S. NUCLEAR REGULATORY COMMISSION
 
==REGION II==


Docket No.: 50-390 License No.: NPF-90  
Docket No.: 50-390 License No.: NPF-90  
Line 269: Line 232:
None   
None   
===Closed===
===Closed===
: [[Closes LER::05000390/LER-2012-005]] LER Automatic Start of Emergency Diesel Generators due to  Failed Transfer of Power to 6.9kV Shutdown Board  (Section 4OA2.3)  
: 05000390/2012-005 LER Automatic Start of Emergency Diesel Generators due to  Failed Transfer of Power to 6.9kV Shutdown Board  (Section 4OA2.3)  


===Opened and Closed===
===Opened and Closed===
Line 276: Line 239:
Attachment   
Attachment   
==LIST OF DOCUMENTS REVIEWED==
==LIST OF DOCUMENTS REVIEWED==
===Procedures===
 
: 1-SI-74-62-B, 18 Month Channel Calibration of Remote Shutdown Control RHR Pump 1B-B
: Miniflow-1FIS-74-24, Rev.0015
: ARI-124-130, Annunciator Response Instruction - Misc, Rev. 15
: BP-213, Managing TVA's Interface with NRC, Rev.0038
: COO-SPP-03.1.1, Corrective Action Program, Rev. 0002
: GO-6, Unit Shutdown from Hot Standby to Cold Shutdown, Rev. 50
: GOI-7, Generic Equipment Operating Guidelines, Rev. 45
: MI-47.001, EHC Tubing Removal and Installation in Support of Turbine Disassembly and Reassembly, Rev. 1
: MI-47.002, EHC Tubing Removal and Installation in Support of Main Turbine Intercept/Stop/Governor/Throttle Valve Maintenance, Rev. 0
: NEDP-22, Operability Determinations and Functional Evaluations, Rev.0014
: NLDP-1, Technical Specifications/Licensee and Amendments, Rev. 8NPG-NEDP-12, Equipment Failure Trending, Rev. 12
: NPG-NEDP-22, Operability Determinations and Functional Eval, Rev. 14
: NPG-NEDP-22-1, Prompt Determination of Operability, Rev. 1
: NPG-NEDP-8, Technical Evaluation for Procurement of Materials and Services, Rev. 21
: NPG-SPP-01.14, Service Request Initiation, Rev.0003
: NPG-SPP-01.2, Administration of Site Technical Procedures, Rev. 9
: NPG-SPP-01.7.1, Employee Concerns Program, Rev.0
: NPG-SPP-02.3, Operating Experience Program, Rev.0005
: NPG-SPP-02.8, Integrated Trend Review, Rev.0003
: NPG-SPP-02.9, CAP Health Monitoring, Rev.007
: NPG-SPP-03.1, Corrective Action Program, Rev.0005
: NPG-SPP-03.1.10, PER Effectiveness Reviews, Rev.0004
: NPG-SPP-03.1.11, NPG Self-Assessment Program, Rev. 1
: NPG-SPP-03.1.12, NPG Benchmarking Program, Rev.0000
: NPG-SPP-03.1.4, Corrective Action Program Screening and Oversight, Rev. 10
: NPG-SPP-03.1.4, Corrective Action Program Screening and Oversight, Rev. 1
: NPG-SPP-03.1.5, Apparent Cause Evaluations, Rev. 5
: NPG-SPP-03.1.6, Root Cause Analysis, Rev. 5
: NPG-SPP-03.1.7, PER Analysis, Actions, Closures and Approvals, Rev. 3
: NPG-SPP-03.1.7, PER Analysis, Actions, Closures and Approvals, Rev. 11
: NPG-SPP-03.4, Maintenance Rule Performance I
ndicator Monitoring, Trending and Reporting - 10CFR50.65, Rev. 1
: NPG-SPP-03.5, Regulatory Reporting Requirements
: NPG-SPP-06.2, Preventive Maintenance, Rev. 0004
: NPG-SPP-07.1, On Line Work Management, Rev. 8NPG-SPP-07.1, On-Line Work Management, Rev. 5 
: Attachment
: NPG-SPP-07.1.4, On Line Prioritization Matrix, Rev. 3
: NPG-SPP-07.7, NPG TCM Role and Oversight of Supplemental Personnel, Rev. 0
: NPG-SPP-09.16.1, System, Component and Program Health, Rev. 0002
: NPG-SPP-09.18.2, Equipment Reliability Classification, Rev.0001
: NPG-SPP-09.18.6, Lifecycle Management Practice for Printed Circuit Boards, Rev.0001
: NPG-SPP-09.18.7, Single Point Vulnerability Review Process, Rev.0002
: NPG-SPP-4.04, Managing the Nuclear Experience Review Program, Rev. 4
: ODM-15.1, Operator Workarounds, Burdens, Challenges, Control Room Deficiencies, and AUO
: Round Deficiencies, Rev. 4 Reporting - 10CFR50.65, Rev.0001
: SOI-78.01, Spent Fuel Pool Cooling and Cleaning System, Rev. 63
: TI-47.01, EHC Tubing Support System Verification, Rev. 0
: WMD-2, Work Management Process Expectations, Rev. 1
: Problem Evaluation Reports Generated
: 678838
: 678107
: 678831
: 680160
: 679397
: 679362
: 680764
: 684998
: 686285
: 686329
: Service Request Generated
: 686688
: 686693
: 686694
: 686695
: 686696
: 686697
: Problem Evaluation Reports Reviewed
: 66067 73262
: 119737
: 151753
: 205438
: 206105
: 227778
: 241525
: 257820
: 297180
: 304173
: 304184
: 304754
: 304851
: 304859
: 305202
: 305281
: 305298
: 307510
: 308693
: 310447
: 313460
: 315495
: 315530
: 315530
: 320932
: 321328
: 322738
: 332853
: 335456
: 335494
: 21990
: 306361
: 341568
: 341645 
: Attachment
: 548548
: 401585
: 247475
: 263575
: 295687
: 316754
: 364577
: 374707
: 402200
: 402283
: 403189
: 21080
: 437085
: 453955
: 487499
: 321990
: 2943
: 353240
: 360788
: 379346
: 390140
: 440368
: 443197
: 478948
: 366905
: 479382
: 573373
: 613924
: 642278
: 350250
: 324586
: 618600
: 619933
: 549880
: 487486
: 298321
: 433863
: 343588
: 349109
: 349292
: 350250
: 350731
: 350921
: 352687
: 355155
: 358538
: 361643
: 366905
: 369840
: 370053
: 373783
: 375008
: 375523
: 379500
: 380817
: 380910
: 386535
: 387781
: 388926
: 391401
: 391471
: 393674
: 394871
: 395494
: 395548
: 396388
: 404512
: 407285
: 409082
: 2907
: 413818
: 415215
: 416466
: 417148
: 417920
: 419909
: 419912
: 20008
: 420807
: 421722
: 422148
: 422689
: 422918
: 425050
: 432883
: 433075
: 440224
: 446649
: 455157
: 455545
: 457556
: 459675
: 460988
: 460998
: 462827
: 463453
: 468860
: 468950
: 471333
: 472391
: 2393
: 477384
: 477527
: 478095
: 479167
: 479385
: 485043
: 485851
: 488825
: 488897
: 489532
: 493932
: 498510
: 498512
: 498515
: 501956
: 502531
: 503144
: 506199
: 506225
: 507645
: 510958
: 511010
: 511469
: 513893
: 514770
: 515307
: 515417
: 515471
: 517095
: 517196
: 520270
: 524952
: 27219
: 527703
: 530224
: 530871
: 531754
: 532688
: 536091
: 538869
: 2890
: 542971
: 546714
: 548593
: 549854
: 550014
: 550570
: 553588
: 554272
: 556259
: 557143
: 559483
: 561230
: 561688
: 564190
: 564190
: 564789 566726`
: 568801
: 568801
: 569203
: 570889
: 577441
: 585187
: 586596
: 587248
: 593388
: 595197
: 595284
: 596406
: 596565
: 597006
: 597043
: 597836
: 598564
: 601154
: 603499
: 606039
: 609015
: 609653
: 614610
: 617221
: 617241
: 618628
: 624075
: 624960
: 624992
: 628580
: 630119
: 630120
: 637287
: 637304
: 637336
: 641674
: 645647
: 648584
: 656988
: 661684
: 669567 
: Attachment
: Service Requests Reviewed
: 118659
: 350789
: 353060
: 428658
===Work Orders===
: Reviewed
: WO 111835793
: WO 111835979
: WO 111843990
: WO 111959711
: WO 112115094
: WO 112165067
: WO 112203744
: WO 112203753
: WO 112208157
: WO 112208179
: WO 112250124
: WO 112259050
: WO 112259189
: WO 112297899
: WO 113455553
: WO 114216763
: WO 112143022
: WO 113139013
===Work Orders===
: Reviewed
: 09-818877-001
: 08-812174-000
: 07-812568-000
: 04-821037-001
: 2141924
: 2162220
: Assessment Reports
: QADP-1, Conduct of Quality Assurance Assessment, Rev. 4
: QADP-2, Internal Audits, Rev. 7
: QADP-4, QA Plan Management, Rev. 3
: QADP-6, QA Escalation, Rev. 0
: QADP-7, Quality Assurance Training, Rev. 3
: QA-WB-11-010, Security Mid-Cycle, dated June 30, 2011
: QA-WB-11-012, EP Mid-Cycle Fleet Assessment of Emergency Preparedness, dated
: June 30, 2011
: QA-WB-11-04, Assessment of Emergency Preparedness Drill, dated February 9, 2011
: WBN-EP-F-12-001, TVA Nuclear Power Group Focused Self-Assessment Report, Revision 1
: CRP-QA-11-001, WBN Nuclear Industry Evaluation Program (NIEP) Mid-cycle Assessment Attachment
: CRP-QA-12-003, WBN Nuclear Industry Evaluation Program (NIEP) Assessment
: CRP-ECP-S-12-001, Employee Concerns Snap-Shot Self-Assessment Report dated September
: 11, 2012 L17-110330-800, TVA Quality Assurance-Nuclear Power Group (NPG) - Watts Bar Nuclear Plant (WBN) - Document Control & Records - Site Audit Report - Audit SSA1104
: L17-111220-800, TVA Quality Assurance-Nuclear Power Group (NPG) - Watts Bar Nuclear Plant (WBN) - Chemistry, Radwaste, Effluent and Environmental Monitoring - Audit Report - SSA1107 L17-120611-800, TVA Quality Assurance-Nuclear Power Group (NPG) - Watts Bar Nuclear Plant (WBN) - Maintenance - Audit Report - SSA1205
: L17-121127-801, NIEP Evaluation of the TVA Nuclear Quality Assurance Program - Site Audit Report SSA1206
: L17-121129-801, TVA Quality Assurance-Nuclear Power Group (NPG) - Watts Bar Nuclear Plant (WBN) - Fire Protection - Audit Report - SSA1214 T34-101222-020, Watts Bar Nuclear Plant - Quality Assurance (QA) - Assessment of
: Chemistry Corrosion Control -
: QA-WB-10-023
: T34-120531-008, Watts Bar Nuclear Plant - Quality Assurance (QA) - Engineering Programs -
: Inservice Testing Assessment -
: QA-WB-12-006 T34-130103-017, Watts Bar Nuclear Plant - Quality Assurance (QA) - Engineering Programs -
: Boric Acid Corrosion Control -
: QA-WB-12-015
: TVA Quality Assurance Master Assessment Schedule 2013 - 2014, Rev. 0
: System Health Reports System Health Report, Residual Heat Removal, 6/1/2012- 9/30/2012
: System Health Report, Residual Heat Removal, 2/1/2012- 5/31/2012
: System Health Report, Residual Heat Removal, 10/1/2011- 01/31/2012
: System Health Report, Residual Heat Removal, 6/1/2011- 9/30/2011
: System Health Report, Residual Heat Removal, 2/1/2011- 5/31/2011
: System Health Report, Residual Heat Removal, 10/1/2010- 1/31//2011
===Calculations===
: T93120417020, Sensitivity Study of Degraded Voltage Relay (DVR) Protection During Motor
: Starting, Rev.0 
: Drawing
: 1-47W848-1, Mechanical Flow Diagram Control Air, Rev. 27 1-45W760-82-5C, Standby Diesel Generating System DG 2B-B, Rev. 13 WBNAPS2135, Material Aging Calculation for Target Rock Valve Components 
(WBNEQ-SQL-002), Rev. 6
: WBNOSG4099, Moderate Energy Line Break Flooding Study, 12
: Other 1-SI-3-90-A, Check Valve Testing During Hot Standby-Auxiliary Feedwater System (Train A), Rev. 15
: 1-SI-3-912, AFW Check Valve Testing During Hot Standby Turbine Driven Flowpath, Rev. 17 1-SI-3-923-A, Auxiliary Feedwater Pump 1A-A Comprehensive Pump Test, Rev. 7 1-SI-92-132, 31 Day Channel Operational Test and full Power Alignment of Source and Intermediate Neutron Flux Channel II
: Attachment
: Compressed Air System (System 32) System Health Report for: Oct 2010 - Jan 2011,
: Feb 2011 - May 2011, June 2011 - Sept 2011, Oct 2011 - Jan 2012, Feb 2012 - May 2012, June 2012 - Sept 2012 in Magne-Blast Circuit Breakers
: NER 920935, Review of II-W-91-017
: NER 940909, WBN NRC
: IN 04-68 Closure Package Nuclear Power Group Performance Improvement,
: TPD-PI, Rev.4
: Operations Watchstander Aggregate Impact Report, 9/2010
: Outage and Non-Outage Operator Burden List, 1/13/2011 Outage and Non-Outage Operator Burden List, 12/9/2010 Outage and Non-Outage Operator Control Room Deficiency List, 1/13/2011
: Outage and Non-Outage Operator Control Room Deficiency List, 12/9/2010
: Outage and Non-Outage Operator Work Around List, 1/13/2011
: Outage and Non-Outage Operator Work Around List, 12/9/2010 PHC Briefing, Singe Point Vulnerability Review Standby Emergency Diesel Generator (System 82) System Health Report for:
: Oct 2010 - Jan 2011, Feb 2011 - May 2011, June 2011 - Sept 2011, Oct 2011 - Jan 2012, Feb 2012 - May 2012, June 2012 - Sept 2012
: TAV 41083, NPG Technical Pre-Job Briefing Checklist
: TVA-SPP-11.8.-4, Expressing Concerns and Differing Views, Revision 0007 Watts Bar CAP Cliff Notes (NPG-SPP-03.1, Corrective Action Program
: WBN Technical Specification Amendment 55
: WBN-SDD-N3-32-4002, Compressed Air System, Rev. 8
: WBN-SDD-N3-63-4001, Safety Injection System, Rev. 27
: WBN-VTD-G080-2240, General Electric Installation and Adjustment of Early A and B Switcher
}}
}}

Revision as of 05:16, 22 June 2019

IR 05000390-13-007, 02/04-8/2013 and 02/19-22/2013, Watts Bar Nuclear Plant, Unit 1, Biennial Inspection of the Identification and Resolution of Problems
ML13098B025
Person / Time
Site: Watts Bar Tennessee Valley Authority icon.png
Issue date: 04/08/2013
From: Hopper G
Reactor Projects Branch 7
To: James Shea
Tennessee Valley Authority
References
IR-13-007
Download: ML13098B025 (22)


Text

April 8, 2013

SUBJECT:

WATTS BAR NUCLEAR PLANT, UN IT 1 - NRC PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000390/2013007

Dear Mr. Shea:

On February 22, 2013, the U. S. Nuclear Regulatory Commission (NRC) completed an inspection at your Watts Bar Nuclear Plant, Unit 1. The enclosed report documents the inspection findings, which were discussed on February 22, 2013, with Mr. Timothy Cleary and other members of your staff.

The inspection was an examination of activities conducted under your license as they relate to the identification and resolution of problems, and compliance with the Commission's rules and regulations and with the conditions of your operating license. Within these areas, the inspection involved examination of selected procedures and representative records, observations of plant equipment and activities, and interviews with personnel.

Based on the inspection sample, the inspection team concluded that the implementation of the corrective action program and overall performance related to identifying, evaluating, and resolving problems at Watts Bar Nuclear Plant was adequate. Licensee identified problems were entered into the corrective action program at an appropriate threshold. Problems were generally prioritized and evaluated commensurate with the safety significance of the problems. Corrective actions were generally implemented in a timely manner commensurate with their importance to safety and addressed the identified causes of problems. Lessons learned from the industry operating experience were generally reviewed and applied when appropriate.

Audits and self-assessments were effectively used to identify problems and appropriate actions.

One NRC identified finding of very low safety significance (Green) was identified during this inspection. The finding did not involve a violation of NRC requirements. If you disagree with the crosscutting aspect assigned to the finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement to the

Regional Administrator, RII, and the NRC Senior Res ident Inspector at the Watts Bar Nuclear Plant, Unit 1. In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electr onically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRC's document system (ADAMS). Adams is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

George T. Hopper, Chief Reactor Projects Branch 7 Division of Reactor Projects

Docket No.: 50-390 License No.: NPF-90

Enclosure:

Inspection Report 05000390/2013007 w/Attachment: Supplemental Information

REGION II==

Docket No.: 50-390 License No.: NPF-90

Report No.: 05000390/2013007 Licensee: Tennessee Valley Authority (TVA)

Facility: Watts Bar Nuclear Plant, Unit 1

Location: Spring City, TN

Dates: February 04 - 08, 2013 February 19 - 22, 2013

Inspectors: N. Staples, Sr. Project Inspector (Team Leader) S. Ninh, Sr. Project Engineer T. Vukovinsky, Reactor Inspector R. Williams, Reactor Inspector

Approved by: George T. Hopper, Chief Reactor Projects Branch 7 Division of Reactor Projects

SUMMARY OF FINDINGS

IR 05000390/2013007; February 04 - 22, 2013; Watts Bar Nuclear Plant, Unit 1; biennial inspection of the identification and resolution of problems.

The inspection was conducted by a senior project inspector, a senior project engineer and two reactor inspectors. One NRC-identified finding of very low safety significance was identified. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for ov erseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process."

Problem Identification and Resolution

The inspectors concluded that, in general, problems were properly identified, evaluated, prioritized, and corrected. The licensee was generally effective at identifying problems and entering them into the corrective action program (CAP) for resolution. Generally, prioritization and evaluation of issues were adequate, formal root cause evaluations for significant problems, and corrective actions specified for problems were consistent with licensee CAP procedures.

Overall, corrective actions developed and implement ed for issues were generally effective and implemented in a timely manner.

The inspectors determined that audits and self-assessments were adequate in identifying deficiencies and areas for improvement in the CAP, and appropriate corrective actions were developed to address the issues identified. Operating experience usage was found to be generally acceptable and integrated into the licensee's processes for performing and managing work, and plant operations.

Based on discussions and interviews conducted with plant employees from various departments, the inspectors determined that personnel at the site felt free to raise safety concerns to management and use the CAP to resolve those concerns.

Cornerstone: Initiating Events

Green: Inspectors identified a finding of very low safety significance for failure to follow procedure BP-259, "Oversight of Supplemental Personnel," Rev. 9. Specifically, during the licensee's review of the vendor instructions for performing maintenance on turbine intercept valve 1-FCV-1-102, the licensee failed to recognize that the vendor instructions were not wholly applicable due to site-specific modifications made on the Electro Hydraulic Control (EHC) system. Consequently, an EHC system leak was identified on valve 1-FCV-1-102 during power ascension at 61% power that led to a manual turbine trip. The issue was entered into the licensee's CAP program as Problem Evaluation Report (PER) 686688.

The finding was determined to be more than minor because it affected the design control attribute of the initiating events cornerstone objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Using the Inspection Manual Chapter 0609, "Significance Determination Process," 3 Phase 1 worksheet, the finding was determined to have very low safety significance because the condition only affected the initiating events cornerstone and did not contribute to both the likelihood of a reactor trip and the likelihood that mitigation equipment or functions will not be available. The finding was determined to have a cross-cutting aspect in Human Performance, Work Practices, in that the licensee did not ensure supervisory and management oversight of work activities, including contractors, such that nuclear safety is supported. (H.4(c)) (4OA2)

REPORT DETAILS

OTHER ACTIVITIES

4OA2 Problem Identification and Resolution

.1 Assessment of the Corrective Action Program

a. Inspection Scope

The inspectors reviewed the licensee's Corrective Action Program (CAP) procedures which described the administrative process for initiating and resolving problems, primarily through the use of Problem Evaluat ion Reports (PERs). To verify that problems were being properly identified, appropriately characterized, and entered into the CAP, the inspectors reviewed PERs that had been issued between January 2011 and February 2013, including a detailed review of selected PERs associated with the following risk-significant systems: Residual Heat Removal (RHR), Emergency Diesel Generators (EDG), and Control Air. Where possible, the inspectors independently verified that the corrective actions were implemented as intended. The inspectors also reviewed selected common cause and generic concerns associated with root cause evaluations to determine if they had been appropriately addressed. The inspectors selected a representative number of PERs that were identified and assigned to the major plant departments, including operations, maintenance, engineering, health physics, chemistry, and security. These PERs were reviewed to assess each department's threshold for identifying and documenting plant problems, thoroughness of evaluations, and adequacy of corrective actions. The inspectors reviewed selected PERs, verified corrective actions were implemented, and attended meetings where PERs were screened for significance to determine whether the licensee was identifying , accurately characterizing, and entering problems into the CAP at an appropriate threshold.

The inspectors conducted plant walkdowns of equipment associated with the selected systems and other plant areas to assess the material condition and to look for any deficiencies that had not been previously entered into the CAP. The inspectors reviewed Service Requests (SR), PERs, maintenance history, completed work orders (WO) for the systems, and reviewed associated system health reports. These reviews were performed to verify that problems were being properly identified, appropriately characterized, and entered into the CAP. Items reviewed generally covered a two-year period of time; however, in accordance with the inspection procedure, a five-year review was performed for selected systems for age-dependent issues.

Control Room walk-downs were also performed to assess the main control room deficiency list and to ascertain if deficiencies were entered into the CAP and tracked to resolution. Operator workarounds (OWA) and operator burden screenings were reviewed, and the inspectors verified compensatory measures for deficient equipment which were being implemented in the field.

The inspectors conducted a detailed review of selected PERs to assess the adequacy of the root cause and apparent cause evaluations of the problems identified. The inspectors reviewed these evaluations against the descriptions of the problem described in the PERs and the guidance in licensee procedure NPG-SPP-03.1.6, "Root Cause Analysis," Rev. 5 and NPG-SPP-03.1.5, "Apparent Cause Evaluations," Rev. 5. The inspectors assessed if the licensee had adequately determined the cause(s) of identified problems, and had adequately addressed operability, reportability, common cause, generic concerns, extent-of-condition, and extent-of-cause. The review also assessed if the licensee had appropriately identified and prioritized corrective actions to prevent recurrence.

The inspectors reviewed selected industry operating experience (OE) items, including NRC generic communications, to verify that they had been appropriately evaluated for applicability and that issues identified through these reviews had been entered into the CAP.

The inspectors reviewed site trend reports, to determine if the licensee effectively trended identified issues and initiated appropriate corrective actions when adverse trends were identified.

The inspectors attended various plant meetings to observe management oversight functions of the corrective action process. These included PER screening meetings, Department Corrective Action Review Board (D-CARB), and the Corrective Action Review Board (CARB).

Documents reviewed are listed in the Attachment.

b. Assessment Identification of Issues

The inspectors determined that the licensee was generally effective in identifying problems and entering them into the CAP and there was an appropriately low threshold for entering issues into the CAP. This conclusion was based on a review of the requirements for initiating SRs as described in licensee procedure NPG-SPP-01.14, "Service Request Initiation", Rev. 3, and management's expectation that employees were encouraged to initiate SRs for any reason. Trending was generally effective in

monitoring equipment performance. Site management was actively involved in the CAP and focused appropriate attention on significant plant issues. Based on reviews and walkdowns of accessible portions of the selected systems, the inspectors determined that system deficiencies were being identified and placed in the CAP.

The inspectors identified the following performance deficiencies. These issues were screened in accordance with Manual Chapter 0612, "Issue Screening," and were determined to be of minor significance and not subject to enforcement action in accordance with the NRC's Enforcement Policy.

On February 12, 2013, the team identified a performance deficiency associated with the

licensee's failure to follow procedure NP G-SPP-03.1.5, "Apparent Cause Evaluations,"

while performing the apparent cause evaluation (ACE) for PER 479167. Specifically, the licensee did not perform an adequate ACE in that the extent of condition (EOC) only looked at the impact of faulted indication lamps on the EDG system. The performance deficiency was considered minor because a subsequent EOC review did not identify any additional safety systems that could be affected by faulty indicating lamps. The licensee initiated SR 686694, ACE 479167 to address this issue. WBN also initiated SR 686693 to address the EOC for IN 94-68 at Watts Bar Nuclear, Sequoyah Nuclear Plant (SR

686696), and Browns Ferry Nuclear Plant (SR 686697).

On February 19, 2013, during system engineering walkdowns, inspectors identified a performance deficiency for not following procedural guidance for anchor point tie-offs.

Specifically, a Unit 2 worker had tied off to a 2 inch conduit for fall protection which was not allowed by procedure 305, "Fall Protect ion Systems." This issue was considered minor because the individual did not challenge the anchor point and no other equipment was affected. PER 680160, U2 Worker Tied Off to two inch Conduit for Fall Protection, was initiated to evaluate what occurred on February 19, 2013, and to determine if any additional corrective actions were needed to address anchorage point tie-offs.

Prioritization and Evaluation of Issues

Based on the review of PERs sampled by the inspection team during the onsite period, the inspectors concluded that problems were generally prioritized and evaluated in accordance with the licensee's CAP procedures as described in the PER significance determination guidance in NPG-SPP-03.1.4, "Corrective Action Program Screening and Oversight," Rev.0010. Each PER was assigned a priority level at the PER screening meeting, and adequate consideration was given to system or component operability and associated plant risk.

The inspectors determined that station personnel had conducted root cause and apparent cause analyses in compliance with the licensee's CAP procedures and assigned cause determinations were appropriate, considering the significance of the issues being evaluated. A variety of formal causal-analysis techniques were used

depending on the type and complexity of the issue consistent with NPG-SPP-03.1.6, "Root Cause Analysis", Rev. 5 and NPG-SPP-03.1.5, "Apparent Cause Evaluations, Rev. 5." Effectiveness of Corrective Actions

Based on a review of corrective action docum ents, interviews with licensee staff, and verification of completed corrective actions, the inspectors determined that, overall, corrective actions were timely, commensurate with the safety significance of the issues, and effective, in that conditions adverse to quality were corrected and non-recurring. For significant conditions adverse to quality, the corrective actions directly addressed the cause and effectively prevented recurrence in that a review of performance indicators, PERs, and effectiveness reviews demonstrated that the significant conditions adverse to quality had not recurred. Effectiveness reviews for corrective actions to prevent recurrence (CAPRs) were sufficient to ensure corrective actions were properly implemented and were effective.

c. Findings

Introduction:

Inspectors identified a Green finding (FIN) for failure to follow procedure BP-259, "Oversight of Supplemental Personnel," Rev. 9. Specifically, the licensee did not recognize that the vendor instructions were not wholly applicable due to site-specific modifications made on the Electro Hydraulic Turbo-generator Controls (EHC) system. Consequently, an EHC system leak was identified on valve 1-FCV-1-102 during power ascension at 61% power that led to a manual turbine trip. The issue was entered into the licensee's CAP program as PER 686688.

Description:

Procedure BP-259 states that the Technical Contract Manager is, in part, responsible for ensuring supplemental (vendor) personnel procedures that perform work in the plant, are prepared, reviewed, revised and approved in accordance with procedure NPG-SPP-01.2, "Administration of Site Technical Procedures." Procedure SPP-01.2, step 3.1.1.D, states in part, "Review procedure prior to use to ensure that potential adherence problems are resolved." During the licensee's review of the vendor instructions for performing maintenance on turbine intercept valve 1-FCV-1-102, the licensee failed to recognize that the vendor instructions were not wholly applicable due to site-specific modifications made on the EHC system. These modifications included the addition of vibration dampening tube support brackets. The vendor instructions did not contain specific steps for the removal of the support brackets nor for their reinstallation. Work was performed utilizing the vendor instructions on three separate occasions in 2006, 2008 and 2009. During one of these evolutions, the tube support brackets were removed but not reinstalled. Subsequently, on April 6, 2011 while performing extent-of-condition inspections initiated due to a prior unrelated EHC tubing failure, personnel noted in the work performed logs that the actuator support brackets on the EHC tubing for valve 1-FCV-1-102 were missing. This work order package was closed without reinstalling the missing support brackets. On May 22, 2011, a through-wall leak was identified on the EHC overspeed protection control tubing near the control block of 1-FCV-1-102. The leak worsened causing the governor and intercept valves to begin drifting closed. The operators commenced a power reduction to 49% power and then initiated a turbine trip, ultimately stabilizing at 6-10% reactor power. The reactor was not tripped due to power levels being below 50% prior to the turbine trip.

Analysis:

The licensee's failure to adequately review the supplemental vendor procedures for work performed on the EHC system in accordance with site procedures was determined to be a performance deficien cy. The inspectors determined that the finding was more than minor because it affected the design control attribute of the initiating events cornerstone objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Using the Inspection Manual Chapter 0609, "Significance Determination Process," Phase 1 worksheet, the finding was determined to have very low safety significance because the condition only affected the initiating events cornerstone and did not contribute to both the likelihood of a reactor trip and the likelihood that mitigation equipment or functions would not be available.

The cause of this finding was directly related to the cross-cutting component of Work Practices in the Human Performance area, in that the licensee did not ensure supervisory and management oversight of work activities, including contractors, such that nuclear safety is supported. (H.4(c))

Enforcement:

Procedure BP-259 states that the Technical Contract Manager is, in part, responsible for ensuring supplemental (vendor) personnel procedures that perform work in plant, are prepared, reviewed, revised and approved in accordance with procedure NPG-SPP-01.2. Procedure NPG-SPP-01.2, step 3.1.1.D, states in part, "Review procedure prior to use to ensure that potential adherence problems are resolved." Contrary to this, on May 22, 2011, inspectors determined that WBN did not follow non-safety related procedure BP-259, in that, the licensee failed to recognize that the vendor instructions were not wholly applicable due to site-specific modifications made on the EHC system. The EHC system is not a safety-related component, procedure BP-259 is not a safety-related procedure, and this finding does not involve enforcement action because no violation of regulatory requirements was identified. Because this finding does not involve a violation and has very low safety significance, it is identified as a FIN. (FIN 05000360/2013007-01, Failure to Follow Procedure BP-529 "Oversight of Supplemental Personnel")

.2 Assessment of the Use of Operating Experience (OE)

a. Inspection Scope

The inspectors examined licensee programs for reviewing industry operating experience, reviewed licensee procedure NPG-SPP-02.3, "Operating Experience Program," reviewed and selected PERs to assess the effectiveness of how external and internal operating experience data was handled at the plant. In addition, the inspectors selected a sample of OE documents (e.g., NRC generic communications, 10 CFR Part 21 reports, licensee event reports, vendor notifications, and plant internal operating experience items, etc.), which had been issued since January 2011 to verify whether the licensee had appropriately evaluated each notification for applicability and whether issues identified through these reviews were entered into the CAP. Documents reviewed are listed in the Attachment.

b. Assessment Based on a review of selected documentation related to operating experience issues, the inspectors determined that the licensee was generally effective in screening operating experience for applicability to the plant. Industry OE was evaluated at either the corporate or plant level depending on the source and type of the document. Relevant information was then forwarded to the applicable department for further action or informational purposes. OE issues requiring action were entered into the CAP for tracking and closure. In addition, operating experience was included in all apparent cause and root cause evaluations in accor dance with licensee procedure NPG-SPP-03.1 "Corrective Action Program", Rev. 5.

c. Findings

No findings were identified.

.3 Assessment of Self-Assessments and Audits

a. Inspection Scope

The inspectors reviewed audit reports and self-assessment reports, including those which focused on problem identification and resolution, to assess the thoroughness and self-criticism of the licensee's audits and self assessments, and to verify that problems identified through those activities were appropriately prioritized and entered into the CAP for resolution in accordance with licensee procedure NPG-SPP-02.1, "Self-Assessment and Benchmark Program", Rev. 0. Documents reviewed are listed in the Attachment.

b. Assessment The inspectors determined that the scopes of assessments and audits were adequate.

Self-assessments were generally detailed and critical, as evidenced by findings consistent with the inspectors' independent review. The inspectors verified that PERs were created to document areas for improvement and findings resulting from the self-assessments, and verified that actions had been completed consistent with those recommendations. Generally, the licensee performed evaluations that were technically accurate. Site trend reports were thorough and a low threshold was established for evaluation of potential trends, as evidenced by the PERs reviewed that were initiated as a result of adverse trends.

c. Findings

No findings were identified.

.4 Assessment of Safety-Conscious Work Environment

a. Inspection Scope

The inspectors randomly interviewed 18 on-site workers regarding their knowledge of the corrective action program at Watts Bar Unit 1 and their willingness to write PERs or raise safety concerns. During technical discussions with members of the plant staff, the inspectors conducted interviews to develop a general perspective of the safety-conscious work environment at the site. The interviews were also conducted to determine if any conditions existed that would cause employees to be reluctant to raise safety concerns. The inspectors review ed the licensee's Employee Concerns Program (ECP) and interviewed the ECP coordinators. Additionally, the inspectors reviewed a sample of completed ECP reports to verify that concerns were being properly reviewed and identified deficiencies were being resolved and entered into the CAP when appropriate. Documents reviewed are listed in the Attachment.

b. Assessment Based on the interviews conducted and the PERs reviewed, the inspectors determined that licensee management emphasized the need for all employees to identify and report problems using the appropriate methods established within the administrative programs, including the CAP and ECP. These methods were readily accessible to all employees.

Based on discussions conducted with a sa mple of plant employees from various departments, the inspectors determined that employees felt free to raise issues, and that management encouraged employees to place issues into the CAP for resolution. The inspectors did not identify any reluctance on the part of the licensee staff to report safety concerns.

c. Findings

No findings were identified.

4OA3 Event Follow-up

.1 (Closed) Licensee Event Report (LER) 05000390/2012-005: Automatic Start of Emergency Diesel Generators due to Failed Transfer of Power to 6.9kV Shutdown Board

On October 16, 2012 at 2330 EDT, Watts Bar Nuclear Plant (WBN-1) licensed operators attempted a manual fast transfer of the 1 B-B 6.9kV Shutdown Board (SDBD) from the normal feeder breaker to the alternate feeder breaker. The transfer was not successful, resulting in the automatic start of the four emergency diesel generators. After the 1 B-B 6.9kV SDBD de-energized and the loads were shed, the alternate feeder breaker closed and re-energized the 1 B-B 6.9kV SDBD. The loads supplied by the 1 B-B 6.9kV SDBD were subsequently reconnected, and required tests were successfully completed to ensure operability of the 1 B-B 6.9kV SDBD. At the time of the event, WBN-1 was in MODE 5 following a refueling outage. Operations personnel promptly entered the appropriate response procedure and re-established power to required loads. The required safety systems functioned as designed. The licensee determined that the likely cause of this event was that plant operators did not ensure the alternate feeder breaker hand-switch was held firmly in the "closed" position while initiating the fast board transfer.

The inspectors reviewed the event and licensee corrective actions taken and no findings were identified. No findings or violations of NRC requirements were identified.

4OA6 Exit

Exit Meeting Summary

On February 22, 2013, the inspectors presented the inspection results to Mr. Tim Cleary, Acting Site-VP, and other members of licensee management. The inspectors confirmed that proprietary information was not provided or examined during the inspection.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee personnel

T. Cleary, Acting Site VP
D. Gronek, Plant Manager
H. Cusick, Employee Concerns Program Manager
T. Morgan, Site Licensing
S. Rymer, Site Engineering
D. Guinn, Manager, Site Licensing
R. Stroud, Site Licensing
J. Hough, Site Licensing
K. Dutton, Director Engineering
R. Cole, CAP Manager, Engineering
S. Ferrell, CAP Analyst
D. Hutchinson, Performance Improvement
J. Deal, Manager, Quality Assurance

NRC personnel

R. Monk, Senior Resident Inspector

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

None

Closed

05000390/2012-005 LER Automatic Start of Emergency Diesel Generators due to Failed Transfer of Power to 6.9kV Shutdown Board (Section 4OA2.3)

Opened and Closed

05000390/2013007-01 FIN Failure to Follow Procedure BP-529 "Oversight of Supplemental Personnel"

Attachment

LIST OF DOCUMENTS REVIEWED