IR 05000298/2007004: Difference between revisions

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{{Adams|number = ML072990072}}
{{Adams
| number = ML072990072
| issue date = 10/25/2007
| title = IR 05000298-07-004; 06/24/2007 - 09/22/07; Cooper Nuclear Station: Radioactive Gaseous and Liquid Effluent Treatment and Monitoring Systems, Identification and Resolution of Problems, Event Followup
| author name = Hay M C
| author affiliation = NRC/RGN-IV/DRP/RPB-C
| addressee name = Minahan S B
| addressee affiliation = Nebraska Public Power District (NPPD)
| docket = 05000298
| license number = DPR-046
| contact person =
| document report number = IR-07-004
| document type = Inspection Report, Letter
| page count = 39
}}


{{IR-Nav| site = 05000298 | year = 2007 | report number = 004 }}
{{IR-Nav| site = 05000298 | year = 2007 | report number = 004 }}
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Gene Mace Nuclear Asset Manager Nebraska Public Power District P.O. Box 98 Brownville, NE 68321John C. McClure, Vice President and General Counsel Nebraska Public Power District P.O. Box 499 Columbus, NE 68602-0499David Van Der Kamp Licensing Manager Nebraska Public Power District P.O. Box 98 Brownville, NE 68321Michael J. Linder, DirectorNebraska Department of Environmental Quality P.O. Box 98922 Lincoln, NE 68509-8922 Nebraska Public Power District-3-ChairmanNemaha County Board of Commissioners Nemaha County Courthouse 1824 N Street Auburn, NE 68305Julia Schmitt, ManagerRadiation Control Program Nebraska Health & Human Services Dept. of Regulation & Licensing Division of Public Health Assurance 301 Centennial Mall, South P.O. Box 95007 Lincoln, NE 68509-5007H. Floyd GilzowDeputy Director for Policy Missouri Department of Natural Resources P. O. Box 176 Jefferson City, MO 65102-0176Director, Missouri State Emergency Management Agency P.O. Box 116 Jefferson City, MO 65102-0116Chief, Radiation and Asbestos Control Section Kansas Department of Health and Environment Bureau of Air and Radiation 1000 SW Jackson, Suite 310 Topeka, KS 66612-1366Melanie Rasmussen, State Liaison Officer/Radiation Control Program Director Bureau of Radiological Health Iowa Department of Public Health Lucas State Office Building, 5th Floor 321 East 12th Street Des Moines, IA 50319John F. McCann, Director, LicensingEntergy Nuclear Northeast Entergy Nuclear Operations, Inc.
Gene Mace Nuclear Asset Manager Nebraska Public Power District P.O. Box 98 Brownville, NE 68321John C. McClure, Vice President and General Counsel Nebraska Public Power District P.O. Box 499 Columbus, NE 68602-0499David Van Der Kamp Licensing Manager Nebraska Public Power District P.O. Box 98 Brownville, NE 68321Michael J. Linder, DirectorNebraska Department of Environmental Quality P.O. Box 98922 Lincoln, NE 68509-8922 Nebraska Public Power District-3-ChairmanNemaha County Board of Commissioners Nemaha County Courthouse 1824 N Street Auburn, NE 68305Julia Schmitt, ManagerRadiation Control Program Nebraska Health & Human Services Dept. of Regulation & Licensing Division of Public Health Assurance 301 Centennial Mall, South P.O. Box 95007 Lincoln, NE 68509-5007H. Floyd GilzowDeputy Director for Policy Missouri Department of Natural Resources P. O. Box 176 Jefferson City, MO 65102-0176Director, Missouri State Emergency Management Agency P.O. Box 116 Jefferson City, MO 65102-0116Chief, Radiation and Asbestos Control Section Kansas Department of Health and Environment Bureau of Air and Radiation 1000 SW Jackson, Suite 310 Topeka, KS 66612-1366Melanie Rasmussen, State Liaison Officer/Radiation Control Program Director Bureau of Radiological Health Iowa Department of Public Health Lucas State Office Building, 5th Floor 321 East 12th Street Des Moines, IA 50319John F. McCann, Director, LicensingEntergy Nuclear Northeast Entergy Nuclear Operations, Inc.


440 Hamilton Avenue White Plains, NY 10601-1813 Nebraska Public Power District-4-Keith G. Henke, PlannerDivision of Community and Public Health Office of Emergency Coordination 930 Wildwood, P.O. Box 570 Jefferson City, MO 65102Paul V. Fleming, Director of Nuclear Safety Assurance Nebraska Public Power District P.O. Box 98 Brownville, NE 68321 Nebraska Public Power District-5-Electronic distribution by RIV:Regional Administrator (EEC)DRP Director (ATH)DRS Director (DDC)DRS Deputy Director (RJC1)Senior Resident Inspector (NHT)Branch Chief, DRP/C (MCH2)Senior Project Engineer, DRP/C (WCW)Team Leader, DRP/TSS (CJP)RITS Coordinator (MSH3)Only inspection reports to the following:DRS STA (DAP)D. Pelton, OEDO RIV Coordinator (DLP)ROPreports CNS Site Secretary (SEF1)SUNSI Review Completed: WCW ADAMS: X Yes __ No Initials: WCW X Publicly Available __ Non-Publicly Available ___ Sensitive X Non-SensitiveR:\_REACTORS\_CNS\2007\CN2007-04RP-NHT.wpdSRI:DRP/CC:SPE:DRP/CC:DRS/EB1C:DRS/PSBC:DRS/OBNHTaylorWCWalkerWBJonesMPShannonATGody/E-WCWalker for/ /RA/ /RA/ /RA/ /RA/10/25/0710/25/0710/22/0710/22/0710/22/07C:DRS/EB2C:DRP/CLJSmithMCHay/RA DLProulx for/ /RA/10/22/0710/25/07OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax Enclosure-1-U.S. NUCLEAR REGULATORY COMMISSIONREGION IV Docket:50-298 License:DPR-46 Report:05000298/2007004 Licensee:Nebraska Public Power District Facility:Cooper Nuclear Station Location:P.O. Box 98 Brownville, Nebraska Dates:June 24 through September 22, 2007 Inspectors:N. Taylor, Senior Resident InspectorM. Chambers, Resident Inspector R. Lantz, Senior Emergency Preparedness Inspector L. Ricketson, P.E., Senior Health Physicist R. Cohen, Resident InspectorApproved By:M. Hay, Branch C, Division of Reactor Projects Enclosure-2-
440 Hamilton Avenue White Plains, NY 10601-1813 Nebraska Public Power District-4-Keith G. Henke, PlannerDivision of Community and Public Health Office of Emergency Coordination 930 Wildwood, P.O. Box 570 Jefferson City, MO 65102Paul V. Fleming, Director of Nuclear Safety Assurance Nebraska Public Power District P.O. Box 98 Brownville, NE 68321 Nebraska Public Power District-5-Electronic distribution by RIV:Regional Administrator (EEC)DRP Director (ATH)DRS Director (DDC)DRS Deputy Director (RJC1)Senior Resident Inspector (NHT)Branch Chief, DRP/C (MCH2)Senior Project Engineer, DRP/C (WCW)Team Leader, DRP/TSS (CJP)RITS Coordinator (MSH3)Only inspection reports to the following:DRS STA (DAP)D. Pelton, OEDO RIV Coordinator (DLP)ROPreports CNS Site Secretary (SEF1)SUNSI Review Completed: WCW ADAMS:
X Yes __ No Initials: WCW X Publicly Available __ Non-Publicly Available ___ Sensitive X Non-SensitiveR:\_REACTORS\_CNS\2007\CN2007-04RP-NHT.wpdSRI:DRP/CC:SPE:DRP/CC:DRS/EB1C:DRS/PSBC:DRS/OBNHTaylorWCWalkerWBJonesMPShannonATGody/E-WCWalker for/ /RA/ /RA/ /RA/ /RA/10/25/0710/25/0710/22/0710/22/0710/22/07C:DRS/EB2C:DRP/CLJSmithMCHay/RA DLProulx for/ /RA/10/22/0710/25/07OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax Enclosure-1-U.S. NUCLEAR REGULATORY COMMISSIONREGION IV Docket:50-298 License:DPR-46 Report:05000298/2007004 Licensee:Nebraska Public Power District Facility:Cooper Nuclear Station Location:P.O. Box 98 Brownville, Nebraska Dates:June 24 through September 22, 2007 Inspectors:N. Taylor, Senior Resident InspectorM. Chambers, Resident Inspector R. Lantz, Senior Emergency Preparedness Inspector L. Ricketson, P.E., Senior Health Physicist R. Cohen, Resident InspectorApproved By:M. Hay, Branch C, Division of Reactor Projects Enclosure-2-


=SUMMARY OF FINDINGS=
=SUMMARY OF FINDINGS=
..................................................-3-
IR 05000298/2007004; 06/24/2007 - 09/22/07; Cooper Nuclear Station: Radioactive Gaseousand Liquid Effluent Treatment And Monitoring Systems, Identification and Resolution of
 
Problems, Event Followup.The report covered a 3-month period of inspection by resident inspectors and region-basedinspectors. Three Green noncited violations and one Green finding were identified. The significance of most findings is indicated by their color (Green, White, Yellow, or Red) using Inspection Manual Chapter 0609, "Significance Determination Process."  Findings for which the significance determination process does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 3, dated July 2000.A.
 
===NRC-Identified and Self-Revealing Findings===
 
===Cornerstone: Mitigating Systems===
: '''Green.'''
The inspectors identified a Green finding regarding the licensee's failure tofollow the requirements of industrial safety procedures. Specifically, licensee personnel violated the requirements of Administrative Procedure 0.36, "Industrial Safety Procedure," and Administrative Procedure 0.36.6, "Monitoring for Industrial Gases," during a chemical injection treatment in the service water system. Specifically, the licensee failed to properly post the hazardous work permit, the individuals performing the work did not review the permit, and licensee personnel did not immediately evacuate the work area as required following a toxic gas release. This issue was entered into the licensee's corrective action program as Condition Report CR-CNS-2007-06421.The finding is more than minor because if left uncorrected it could become a moresignificant safety concern in that failure to follow industrial safety procedures during chlorine dioxide injections could put personnel at significant risk of injury and could have resulted in a larger toxic gas release in the intake structure, inhibiting the operators'
ability to access safety related equipment to mitigate the consequences of an accident.
 
Using Inspection Manual Chapter 0609, Appendix A, "Determining the Significance of Reactor Inspection Findings for At-Power Situations," the finding was determined to be of very low safety significance because it did not result in a loss of safety function for any mitigating system. The cause of this finding is related to the human performance cross cutting component of work practices in that licensee personnel did not follow the requirements of industrial safety procedures as required (H.4(b)). (Section 4OA3)
: '''Green.'''
The inspectors identified a noncited violation of 10 CFR 50, Appendix B,Criterion XVI, "Corrective Action," regarding the licensee's failure to promptly identify and correct a condition adverse to quality. Specifically, a degraded condition that was discovered in the service water supply piping to Diesel Generator 2 on August 16, 2007, was not evaluated for its effect on the operability of Diesel Generator 2 until prompted Enclosure-4-by inspectors on August 17, 2007. As a result, additional unavailability time wasnecessary to repair the degraded condition. This issue was entered into the licensee's corrective action program as Condition Report CR-CNS-2007-05590.The finding is more than minor because if left uncorrected, the flow erosion of the DieselGenerator 2 service water supply piping could have become a more significant safety concern. Using Inspection Manual Chapter 0609, Appendix A, "Determining the Significance of Reactor Inspection Findings for At-Power Situations," the finding was determined to be of very low safety significance because it did not represent an actual loss of safety function of the diesel generator for greater than its technical specification allowed outage time. The cause of this finding is related to the problem identification and resolution cross cutting component of corrective action program in that the licensee did not correct the degraded condition of the Diesel Generator 2 service water piping in a timely manner (P.1(a)). (Section 4OA2)
 
===Cornerstone: Emergency Preparedness===
: '''Green.'''
The inspectors identified a noncited violation of 10 CFR 50.47 (b)(4) regardingthe licensee's failure to establish adequate procedural guidance to implement the emergency plan. Specifically, Emergency Plan Implementing Procedure 5.7.1,
"Emergency Classification", Revision 35, contained inadequate procedural guidance in that it did not identify any specific entry criteria for Emergency Action Level 5.1.2. This issue was entered into the licensee's corrective action program as Condition Report CR-CNS-2007-05135.The finding is more than minor because it is associated with the EmergencyPreparedness cornerstone attribute of procedural quality and affects the associated cornerstone objective to ensure that the licensee is capable of implementing adequate measures to protect the health and safety of the public in the event of a radiological emergency. Using Inspection Manual Chapter 0609, Appendix B, "Emergency Preparedness Significance Determination Process," the finding was determined to be of very low safety significance since the EAL classification process that was in place prior to August 30, 2007 could have resulted in a failure to declare a Notification of Unusual Event when it should have been declared. The cause of this finding is related to the human performance cross cutting component of resources in that complete and accurate procedures were not adequately maintained to support the emergency plan (H.2(c)).   (Section 4OA3)
 
===Cornerstone: Public Radiation Safety===
: '''Green.'''
The inspector identified a noncited violation of 10 CFR 20.1302(a) because thelicensee's surveys of effluents containing radioactive particulates originating in the multi-purpose facility were not adequate to ensure compliance with the dose limits for individual members of the public required by 10 CFR 20.1301. The surveys were not adequate because the configuration of the radioactive effluent monitoring system in the multi-purpose facility was changed in 2007, and the sampling lines in the new configuration were not analyzed for line loss. The licensee documented the situation in the corrective action program and declared the multi-purpose facility effluent monitoring system inoperable. Further corrective action is being evaluated.
 
Enclosure-5-The finding is greater than minor because it is associated with the Public RadiationSafety Cornerstone attribute of equipment and instrumentation and affects the cornerstone objective in that the failure to perform adequate surveys of radioactive effluents could result in increased public dose. When processed through the Public Radiation Safety Significance Determination Process, the finding was determined to be of very low safety significance because it: (1) was not a radioactive material control finding, (2) was an effluent release program finding, (3) impaired the licensee's ability to assess dose, (4) it did not result in a failure to assess dose, (5) did not result in public doses that exceeded the values of 10 CFR Part 50, Appendix I, or 10 CFR 20.1301(d).
 
In addition, this finding had cross-cutting aspects in the area of human performance and the component of resources because the licensee did not ensure complete, accurate, and up-to-date design documentation requests and specifications were supplied to outsourced engineering providers. (H.2.(c)) (Section 2PS1)
Enclosure-6-


=REPORT DETAILS=
=REPORT DETAILS=
........................................................-6-
Summary of Plant StatusThe plant began the inspection period at 100 percent power. On August 11, 2007, reactorpower was reduced to approximately 70 percent for a planned rod pattern exchange and surveillance testing. During the power ascension, one of four circulating water discharge valves stuck shut, and as a result the licensee held power at approximately 93 percent. On August 13, 2007, the licensee returned to full power and remained there for the rest of the inspection period.


==REACTOR SAFETY==
==REACTOR SAFETY==
.......................................................-6-1R04 Equipment Alignment...........................................-6-1R05 Fire Protection................................................-7-1R11 Licensed Operator Requalification.................................-8-1R12 Maintenance Rule.............................................-8-1R13 Maintenance Risk Assessments and Emergent Work Evaluation.........-9-1R15 Operability Evaluations.........................................-9-1R19 Postmaintenance Testing......................................-10-1R22 Surveillance Testing...........................................-11-1EP2Alert Notification System Testing.................................-11-1EP3Emergency Response Organization Augmentation Testing.............-12-1EP5Correction of Emergency Preparedness Weaknesses and Deficiencies...-12-RADIATION SAFETY.....................................................-12-2OS1Access Control to Radiologically Significant Areas...................-13-2OS2ALARA Planning and Controls...................................-14-2PS1Radioactive Gaseous and Liquid Effluent Treatment and Monitoring Systems-15-OTHER ACTIVITIES......................................................-17-4OA1Performance Indicator Verification................................-17-4OA2 Problem Identification and Resolution.............................-18-4OA3Event Follow-up..............................................-21-4OA6Meeting, Including Exit.........................................-26-ATTACHMENT: 
Cornerstones:  Initiating Events, Mitigating Systems, Barrier Integrity, and EmergencyPreparedness1R04 Equipment Alignment (71111.04Q)
 
===.1 Partial System Walkdown===
 
====a. Inspection Scope====
The inspectors:
: (1) walked down portions of the two risk important systems listed belowand reviewed plant procedures and documents to verify that critical portions of the selected systems were correctly aligned; and
: (2) compared deficiencies identified during the walkdown to the licensee's UFSAR and the licensee's CAP to ensure problems were being identified and corrected. *August 7, 2007, Division II Residual Heat Removal (RHR) during plannedmaintenance on Div 1RHR*September 18, 2007, Reactor Core Isolation Cooling (RCIC) during HighPressure Coolant Injection MaintenanceThe inspectors completed two samples.


=SUPPLEMENTAL INFORMATION=
====b. Findings====
No findings of significance were identified.
 
===.2 Complete System Walkdown===
{{IP sample|IP=IP 71111.04S}}
 
====a. Inspection Scope====
The inspectors:
: (1) reviewed plant procedures, drawings, the UFSAR, TSs, and vendormanuals to determine the correct alignment of the Reactor Building Ventilation System;
: (2) reviewed outstanding design issues, operator workarounds, and UFSAR documents 
-7-to determine if open issues affected the functionality of the Reactor Building VentilationSystem; and
: (3) verified that the licensee was identifying and resolving equipment alignment problems.*September 19, 2007, Reactor Building Ventilation System The inspectors completed one sample.
 
====b. Findings====
No findings of significance were identified.
{{a|1R05}}
==1R05 Fire Protection==
Fire Protection Tours (71111.05Q)


==KEY POINTS OF CONTACT==
====a. Inspection Scope====
................................................A-1
The inspectors walked down the six plant areas listed below to assess the materialcondition of active and passive fire protection features and their operational lineup and readiness. The inspectors:
==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==
: (1) verified that transient combustibles and hot work activities were controlled in accordance with plant procedures;
...........................A-2
: (2) observed the condition of fire detection devices to verify they remained functional;
==LIST OF DOCUMENTS REVIEWED==
: (3) observed fire suppression systems to verify they remained functional and that access to manual actuators was unobstructed;
..........................................A-2
: (4) verified that fire extinguishers and hose stations were provided at their designated locations and that they were in a satisfactory condition; (5)verified that passive fire protection features (electrical raceway barriers, fire doors, fire dampers, steel fire proofing, penetration seals, and oil collection systems) were in a satisfactory material condition;
==LIST OF ACRONYMS==
: (6) verified that adequate compensatory measures were established for degraded or inoperable fire protection features and that the compensatory measures were commensurate with the significance of the deficiency; and
......................................................A-8
: (7) reviewed the UFSAR to determine if the licensee identified and corrected fire protection problems. *July 11, 2007, Fire Zone 20A, Service Water Pump Room*July 25, 2007, Fire Zone 9B, Cable Expansion Room
Enclosure-3-SUMMARY
: [[OF]] [[]]
FINDINGSIR 05000298/2007004; 06/24/2007 - 09/22/07; Cooper Nuclear Station: Radioactive Gaseousand Liquid Effluent Treatment And Monitoring Systems, Identification and Resolution of
Problems, Event Followup.The report covered a 3-month period of inspection by resident inspectors and region-basedinspectors. Three Green noncited violations and one Green finding were identified. The
significance of most findings is indicated by their color (Green, White, Yellow, or Red) using
Inspection Manual Chapter 0609, "Significance Determination Process."  Findings for which the
significance determination process does not apply may be Green or be assigned a severity
level after
: [[NRC]] [[management review. The]]
NRC's program for overseeing the safe operation of
commercial nuclear power reactors is described in
: [[NUR]] [[]]
EG-1649, "Reactor Oversight Process,"
Revision 3, dated July
: [[2000.A.N]] [[]]
RC-Identified and Self-Revealing FindingsCornerstone: Mitigating Systems*Green. The inspectors identified a Green finding regarding the licensee's failure tofollow the requirements of industrial safety procedures. Specifically, licensee personnel
violated the requirements of Administrative Procedure 0.36, "Industrial Safety
Procedure," and Administrative Procedure 0.36.6, "Monitoring for Industrial Gases,"
during a chemical injection treatment in the service water system. Specifically, the
licensee failed to properly post the hazardous work permit, the individuals performing
the work did not review the permit, and licensee personnel did not immediately evacuate
the work area as required following a toxic gas release. This issue was entered into the
licensee's corrective action program as Condition Report
: [[CR]] [[-]]
CNS-2007-06421.The finding is more than minor because if left uncorrected it could become a moresignificant safety concern in that failure to follow industrial safety procedures during
chlorine dioxide injections could put personnel at significant risk of injury and could have
resulted in a larger toxic gas release in the intake structure, inhibiting the operators'
ability to access safety related equipment to mitigate the consequences of an accident.
Using Inspection Manual Chapter 0609, Appendix A, "Determining the Significance of
Reactor Inspection Findings for At-Power Situations," the finding was determined to be
of very low safety significance because it did not result in a loss of safety function for
any mitigating system. The cause of this finding is related to the human performance
cross cutting component of work practices in that licensee personnel did not follow the
requirements of industrial safety procedures as required (H.4(b)).  (Section
: [[4OA]] [[3)  *Green. The inspectors identified a noncited violation of 10]]
CFR 50, Appendix B,Criterion XVI, "Corrective Action," regarding the licensee's failure to promptly identify
and correct a condition adverse to quality. Specifically, a degraded condition that was
discovered in the service water supply piping to Diesel Generator 2 on August 16, 2007,
was not evaluated for its effect on the operability of Diesel Generator 2 until prompted
Enclosure-4-by inspectors on August 17, 2007. As a result, additional unavailability time wasnecessary to repair the degraded condition. This issue was entered into the licensee's
corrective action program as Condition Report
: [[CR]] [[-]]
CNS-2007-05590.The finding is more than minor because if left uncorrected, the flow erosion of the DieselGenerator 2 service water supply piping could have become a more significant safety
concern. Using Inspection Manual Chapter 0609, Appendix A, "Determining the
Significance of Reactor Inspection Findings for At-Power Situations," the finding was
determined to be of very low safety significance because it did not represent an actual
loss of safety function of the diesel generator for greater than its technical specification
allowed outage time. The cause of this finding is related to the problem identification and
resolution cross cutting component of corrective action program in that the licensee did
not correct the degraded condition of the Diesel Generator 2 service water piping in a
timely manner (P.1(a)).  (Section
: [[4OA]] [[2)Cornerstone: Emergency Preparedness*Green. The inspectors identified a noncited violation of 10]]
CFR 50.47 (b)(4) regardingthe licensee's failure to establish adequate procedural guidance to implement the
emergency plan. Specifically, Emergency Plan Implementing Procedure 5.7.1,
"Emergency Classification", Revision 35, contained inadequate procedural guidance in
that it did not identify any specific entry criteria for Emergency Action Level 5.1.2. This
issue was entered into the licensee's corrective action program as Condition Report
: [[CR]] [[-]]
CNS-2007-05135.The finding is more than minor because it is associated with the EmergencyPreparedness cornerstone attribute of procedural quality and affects the associated
cornerstone objective to ensure that the licensee is capable of implementing adequate
measures to protect the health and safety of the public in the event of a radiological
emergency. Using Inspection Manual Chapter 0609, Appendix B, "Emergency
Preparedness Significance Determination Process," the finding was determined to be of
very low safety significance since the EAL classification process that was in place prior
to August 30, 2007 could have resulted in a failure to declare a Notification of Unusual
Event when it should have been declared. The cause of this finding is related to the
human performance cross cutting component of resources in that complete and
accurate procedures were not adequately maintained to support the emergency plan
(H.2(c)).  (Section
: [[4OA]] [[3)Cornerstone: Public Radiation Safety*Green. The inspector identified a noncited violation of 10]]
CFR 20.1302(a) because thelicensee's surveys of effluents containing radioactive particulates originating in the
multi-purpose facility were not adequate to ensure compliance with the dose limits for
individual members of the public required by 10 CFR 20.1301. The surveys were not
adequate because the configuration of the radioactive effluent monitoring system in the
multi-purpose facility was changed in 2007, and the sampling lines in the new
configuration were not analyzed for line loss. The licensee documented the situation in
the corrective action program and declared the multi-purpose facility effluent monitoring
system inoperable. Further corrective action is being evaluated.
Enclosure-5-The finding is greater than minor because it is associated with the Public RadiationSafety Cornerstone attribute of equipment and instrumentation and affects the
cornerstone objective in that the failure to perform adequate surveys of radioactive
effluents could result in increased public dose. When processed through the Public
Radiation Safety Significance Determination Process, the finding was determined to be
of very low safety significance because it: (1) was not a radioactive material control
finding, (2) was an effluent release program finding, (3) impaired the licensee's ability to
assess dose, (4) it did not result in a failure to assess dose, (5) did not result in public
doses that exceeded the values of
: [[10 CFR]] [[Part 50, Appendix I, or 10]]
CFR 20.1301(d).
In addition, this finding had cross-cutting aspects in the area of human performance and
the component of resources because the licensee did not ensure complete, accurate,
and up-to-date design documentation requests and specifications were supplied to
outsourced engineering providers. (H.2.(c)) (Section 2PS1)
Enclosure-6-REPORT
: [[DETAIL]] [[]]
SSummary of Plant StatusThe plant began the inspection period at 100 percent power. On August 11, 2007, reactorpower was reduced to approximately 70 percent for a planned rod pattern exchange and
surveillance testing. During the power ascension, one of four circulating water discharge valves
stuck shut, and as a result the licensee held power at approximately 93 percent. On
August 13, 2007, the licensee returned to full power and remained there for the rest of the
inspection period.
: [[1.REACT]] [[]]
: [[OR]] [[]]
: [[SAFET]] [[]]
YCornerstones:  Initiating Events, Mitigating Systems, Barrier Integrity, and EmergencyPreparedness1R04 Equipment Alignment (71111.04Q)  .1Partial System Walkdown    a.Inspection ScopeThe inspectors:  (1) walked down portions of the two risk important systems listed belowand reviewed plant procedures and documents to verify that critical portions of the
selected systems were correctly aligned; and (2) compared deficiencies identified during
the walkdown to the licensee's
: [[UFSAR]] [[and the licensee's]]
CAP to ensure problems were
being identified and corrected. *August 7, 2007, Division
: [[II]] [[Residual Heat Removal (]]
: [[RHR]] [[) during plannedmaintenance on Div]]
: [[1RHR]] [[*September 18, 2007, Reactor Core Isolation Cooling (]]
: [[RCIC]] [[) during HighPressure Coolant Injection MaintenanceThe inspectors completed two samples. b.FindingsNo findings of significance were identified.  .2Complete System Walkdown (71111.04S)    a.Inspection ScopeThe inspectors:  (1) reviewed plant procedures, drawings, the]]
: [[UFSAR]] [[,]]
TSs, and vendormanuals to determine the correct alignment of the Reactor Building Ventilation System;
(2) reviewed outstanding design issues, operator workarounds, and
: [[UFS]] [[]]
AR documents
Enclosure-7-to determine if open issues affected the functionality of the Reactor Building VentilationSystem; and (3) verified that the licensee was identifying and resolving equipment
alignment problems.*September 19, 2007, Reactor Building Ventilation System
The inspectors completed one sample. b.FindingsNo findings of significance were identified.1R05 Fire Protection  Fire Protection Tours (71111.05Q)    a.Inspection ScopeThe inspectors walked down the six plant areas listed below to assess the materialcondition of active and passive fire protection features and their operational lineup and
readiness. The inspectors: (1) verified that transient combustibles and hot work
activities were controlled in accordance with plant procedures; (2) observed the
condition of fire detection devices to verify they remained functional; (3) observed fire
suppression systems to verify they remained functional and that access to manual
actuators was unobstructed; (4) verified that fire extinguishers and hose stations were
provided at their designated locations and that they were in a satisfactory condition; (5)
verified that passive fire protection features (electrical raceway barriers, fire doors, fire
dampers, steel fire proofing, penetration seals, and oil collection systems) were in a
satisfactory material condition; (6) verified that adequate compensatory measures were
established for degraded or inoperable fire protection features and that the
compensatory measures were commensurate with the significance of the deficiency;
and (7) reviewed the
: [[UFS]] [[]]
AR to determine if the licensee identified and corrected fire
protection problems. *July 11, 2007, Fire Zone 20A, Service Water Pump Room*July 25, 2007, Fire Zone 9B, Cable Expansion Room
*July 25, 2007, Fire Zone 1B, Core Spray Pump Room
*July 25, 2007, Fire Zone 1B, Core Spray Pump Room
*July 25, 2007, Fire Zone 1G, Hydraulic Drive Pump Area
*July 25, 2007, Fire Zone 1G, Hydraulic Drive Pump Area
*August 10, 2007, Fire Zone 20A, Service Water Pump Room During B StrainerCleaning*September 20, 2007, Fire Zone 1A,
*August 10, 2007, Fire Zone 20A, Service Water Pump Room During B Strainer Cleaning*September 20, 2007, Fire Zone 1A, RCIC and Core Spray Pump RoomDocuments reviewed by the inspectors included:
: [[RC]] [[]]
Administrative Procedure 0.23, CNS Fire Protection Plan, Revision 49 The inspectors completed six samples.
IC and Core Spray Pump RoomDocuments reviewed by the inspectors included:
 
Administrative Procedure 0.23, CNS Fire Protection Plan, Revision 49
-8-
The inspectors completed six samples.
 
Enclosure-8-   b. FindingsNo findings of significance were identified.1R11 Licensed Operator Requalification (71111.11Q)     a.Inspection ScopeThe inspectors observed testing and training of senior reactor operators and reactoroperators to identify deficiencies and discrepancies in the training, to assess operator
====b. Findings====
performance, and to assess the evaluator's critique. The inspectors' observations were
No findings of significance were identified.
performed on August 10, 2007 by monitoring control rod manipulation during a
{{a|1R11}}
scheduled downpower and an effectiveness review of requalification training.The inspectors completed one sample. b. FindingsNo findings of significance were identified.1R12Maintenance Rule (711111.12Q)     a.Inspection ScopeThe inspectors reviewed the maintenance effectiveness performance issues listed belowto: (1) verify the appropriate handling of structure, system, and component (SSC)
==1R11 Licensed Operator Requalification (71111.11Q)==
performance or condition problems; (2) verify the appropriate handling of degraded SSC
 
functional performance; (3) evaluate the role of work practices and common cause
====a. Inspection Scope====
problems; and (4) evaluate the handling of SSC issues reviewed under the requirements
The inspectors observed testing and training of senior reactor operators and reactoroperators to identify deficiencies and discrepancies in the training, to assess operator performance, and to assess the evaluator's critique. The inspectors' observations were performed on August 10, 2007 by monitoring control rod manipulation during a scheduled downpower and an effectiveness review of requalification training.The inspectors completed one sample.
of the maintenance rule,
 
: [[10 CFR]] [[Part 50, Appendix B, and the]]
====b. Findings====
TSs.*September 4, 2007, CRD-V-101(25-27) leakage on May 19, 2007*September 4, 2007, Failure of Division 1 Service Water Strainer on            August 1, 2007Documents reviewed by the inspectors included:
No findings of significance were identified.
*Functional Failure Evaluations for functions
{{a|1R12}}
: [[CRD]] [[-F02A and]]
==1R12 Maintenance Rule (711111.12Q)==
: [[CRD]] [[-V-F03a*Functional Failure Evaluations for functions]]
 
: [[SW]] [[-F01A and]]
====a. Inspection Scope====
SW01C
The inspectors reviewed the maintenance effectiveness performance issues listed belowto:
*CR-CNS-2007-05210The inspectors completed two samples. b. FindingsNo findings of significance were identified.
: (1) verify the appropriate handling of structure, system, and component (SSC)performance or condition problems;
Enclosure-9-1R13Maintenance Risk Assessments and Emergent Work Evaluation (71111.13)     a.Inspection Scope The inspectors reviewed the three maintenance activities listed below to verify:  (1)performance of risk assessments when required by 10 CFR 50.65 (a)(4) and licensee
: (2) verify the appropriate handling of degraded SSC functional performance;
procedures prior to changes in plant configuration for maintenance activities and plant
: (3) evaluate the role of work practices and common cause problems; and
operations; (2) the accuracy, adequacy, and completeness of the information
: (4) evaluate the handling of SSC issues reviewed under the requirements of the maintenance rule, 10 CFR Part 50, Appendix B, and the TSs.*September 4, 2007, CRD-V-101(25-27) leakage on May 19, 2007*September 4, 2007, Failure of Division 1 Service Water Strainer on            August 1, 2007Documents reviewed by the inspectors included:
considered in the risk assessment; (3) that the licensee recognized, and/or entered as
*Functional Failure Evaluations for functions CRD-F02A and CRD-V-F03a*Functional Failure Evaluations for functions SW-F01A and SW01C
applicable, the appropriate licensee-established risk category according to the risk
*CR-CNS-2007-05210The inspectors completed two samples.
assessment results and licensee procedures; and (4) the licensee identified and
 
corrected problems related to maintenance risk assessments.*June 28, 2007, Reactor Vessel Level Control System Troubleshooting*August 7, 2007, Work on
====b. Findings====
: [[RHR]] [[-]]
No findings of significance were identified.
MOV-13A
 
-9-1R13Maintenance Risk Assessments and Emergent Work Evaluation (71111.13)
 
====a. Inspection Scope====
The inspectors reviewed the three maintenance activities listed below to verify:  (1)performance of risk assessments when required by 10 CFR 50.65 (a)(4) and licensee procedures prior to changes in plant configuration for maintenance activities and plant operations;
: (2) the accuracy, adequacy, and completeness of the information considered in the risk assessment;
: (3) that the licensee recognized, and/or entered as applicable, the appropriate licensee-established risk category according to the risk assessment results and licensee procedures; and
: (4) the licensee identified and corrected problems related to maintenance risk assessments.*June 28, 2007, Reactor Vessel Level Control System Troubleshooting*August 7, 2007, Work on RHR-MOV-13A
*August 13, 2007, Emergent Downpower for Circulating Water System ManipulationDocuments reviewed by the inspectors included:
*August 13, 2007, Emergent Downpower for Circulating Water System ManipulationDocuments reviewed by the inspectors included:
*Work Order (WO) 4572910*Administrative Procedure 0.49, "Schedule Risk Assessment," Rev. 19
*Work Order (WO) 4572910*Administrative Procedure 0.49, "Schedule Risk Assessment," Rev. 19
*Administrative Procedure O-PROTECT-EQP, "Protected Equipment Program,"Rev. 5*CR-CNS-2007-05331The inspectors completed three samples.     b.FindingsNo findings of significance were identified.1R15 Operability Evaluations (71111.15)     a.Inspection Scope The inspectors: (1) reviewed operator shift logs, emergent work documentation,deferred modifications, and standing orders to determine if an operability evaluation was
*Administrative Procedure O-PROTECT-EQP, "Protected Equipment Program,"Rev. 5*CR-CNS-2007-05331The inspectors completed three samples.
warranted for degraded components; (2) referred to the
 
: [[UFS]] [[]]
====b. Findings====
AR and other design basis
No findings of significance were identified.
documents to review the technical adequacy of licensee operability evaluations; (3)
{{a|1R15}}
evaluated compensatory measures associated with operability evaluations; (4)
==1R15 Operability Evaluations (71111.15)==
determined degraded component impact on any TSs; (5) used the Significance
 
Determination Process to evaluate the risk significance of degraded or inoperable
====a. Inspection Scope====
equipment; and (6) verified that the licensee has identified and implemented appropriate
The inspectors:
corrective actions associated with degraded components.
: (1) reviewed operator shift logs, emergent work documentation,deferred modifications, and standing orders to determine if an operability evaluation was warranted for degraded components;
Enclosure-10-The following equipment performance issues were reviewed: *July 10, 2007, Diesel Generator (DG) 1 Operability with High Service WaterSediment Levels*August 15, 2007, DG 2 Service Water Piping Leak
: (2) referred to the UFSAR and other design basis documents to review the technical adequacy of licensee operability evaluations; (3)evaluated compensatory measures associated with operability evaluations; (4)determined degraded component impact on any TSs;
*August 30, 2007,
: (5) used the Significance Determination Process to evaluate the risk significance of degraded or inoperable equipment; and
: [[DG]] [[Lubricating Oil and Jacket Water Heat Exchanger TubePlugs Over-torqued*September 7, 2007,]]
: (6) verified that the licensee has identified and implemented appropriate corrective actions associated with degraded components.
DG 1 Operability Common Cause Review
 
-10-The following equipment performance issues were reviewed: *July 10, 2007, Diesel Generator (DG) 1 Operability with High Service WaterSediment Levels*August 15, 2007, DG 2 Service Water Piping Leak
*August 30, 2007, DG Lubricating Oil and Jacket Water Heat Exchanger TubePlugs Over-torqued*September 7, 2007, DG 1 Operability Common Cause Review
*September 11, 2007, DG 1 Operability Following Day Tank Level Control SystemFailureDocuments reviewed by the inspectors included:
*September 11, 2007, DG 1 Operability Following Day Tank Level Control SystemFailureDocuments reviewed by the inspectors included:
*CR-CNS-2007-05571*CR-CNS-2007-05875
*CR-CNS-2007-05571*CR-CNS-2007-05875
*CR-CNS-2007-04688
*CR-CNS-2007-04688
*CR-CNS-2007-06143The inspectors completed five samples.     b.FindingsNo findings of significance were identified.1R19 Postmaintenance Testing (71111.19)     a.Inspection ScopeThe inspectors selected four post-maintenance tests associated with the maintenanceactivities listed below for risk significant systems or components. For each item, the
*CR-CNS-2007-06143The inspectors completed five samples.
inspectors: (1) reviewed the applicable licensing basis and/or design basis documentsto determine the safety functions; (2) evaluated the safety functions that may have been
 
affected by the maintenance activity; and (3) reviewed the test procedure to ensure it
====b. Findings====
adequately tested the safety function that may have been affected. The inspectors
No findings of significance were identified.
either witnessed or reviewed test data to verify that acceptance criteria were met, plant
{{a|1R19}}
impacts were evaluated, test equipment was calibrated, procedures were followed,
==1R19 Postmaintenance Testing (71111.19)==
jumpers were properly controlled, the test data results were complete and accurate, the
 
test equipment was removed, the system was properly re-aligned, and deficiencies
====a. Inspection Scope====
during testing were documented. The inspectors also reviewed the
The inspectors selected four post-maintenance tests associated with the maintenanceactivities listed below for risk significant systems or components. For each item, the inspectors:
: [[UFS]] [[]]
: (1) reviewed the applicable licensing basis and/or design basis documentsto determine the safety functions;
AR to
: (2) evaluated the safety functions that may have been affected by the maintenance activity; and
determine if the licensee identified and corrected problems related to postmaintenance
: (3) reviewed the test procedure to ensure it adequately tested the safety function that may have been affected. The inspectors either witnessed or reviewed test data to verify that acceptance criteria were met, plant impacts were evaluated, test equipment was calibrated, procedures were followed, jumpers were properly controlled, the test data results were complete and accurate, the test equipment was removed, the system was properly re-aligned, and deficiencies during testing were documented. The inspectors also reviewed the UFSAR to determine if the licensee identified and corrected problems related to postmaintenance testing. *August 3, 2007, Post-Accident Sampling System following relief valvereplacements and valve rebuilds*August 7, 2007, RHR-MOV-13A test following motor pinion inspection/repair
testing. *August 3, 2007, Post-Accident Sampling System following relief valvereplacements and valve rebuilds*August 7, 2007,
: [[RHR]] [[-]]
MOV-13A test following motor pinion inspection/repair
*August 10, 2007, Service Water B zurn strainer following inspection
*August 10, 2007, Service Water B zurn strainer following inspection
*August 16, 2007, DG 2 Service Water piping repairThe inspectors completed four samples.
*August 16, 2007, DG 2 Service Water piping repairThe inspectors completed four samples.
Enclosure-11-     b.FindingsNo findings of significance were identified.1R22 Surveillance Testing (71111.22)   a.Inspection ScopeThe inspectors reviewed the
 
: [[UFSAR]] [[, procedure requirements, and]]
-11-
TSs to ensure thatthe three surveillance activities listed below demonstrated that the SSCs tested were
 
capable of performing their intended safety functions. The inspectors either witnessed
====b. Findings====
or reviewed test data to verify that the following significant surveillance test attributes
No findings of significance were identified.
were adequate: (1) preconditioning; (2) evaluation of testing impact on the plant; (3)
{{a|1R22}}
acceptance criteria; (4) test equipment; (5) procedures; (6) jumper/lifted lead controls;
==1R22 Surveillance Testing (71111.22)==
(7) test data; (8) testing frequency and method demonstrated TS operability; (9) test
 
equipment removal; (10) restoration of plant systems; (11) fulfillment of American
====a. Inspection Scope====
Society Mechanical Engineers Code requirements; (12) engineering evaluations, root
The inspectors reviewed the UFSAR, procedure requirements, and TSs to ensure thatthe three surveillance activities listed below demonstrated that the SSCs tested were capable of performing their intended safety functions. The inspectors either witnessed or reviewed test data to verify that the following significant surveillance test attributes were adequate:
causes, and bases for returning tested SSCs not meeting the test acceptance criteria
: (1) preconditioning;
were correct; (13) reference setting data;  and (14) annunciators and alarms setpoints.
: (2) evaluation of testing impact on the plant; (3)acceptance criteria;
The inspectors also verified that the licensee identified and implemented any needed
: (4) test equipment;
corrective actions associated with the surveillance testing.*August 1, 2007, DG Fuel Oil Availability*August 6, 2007, Standby Liquid Control Tank Sample
: (5) procedures;
*August 7, 2007,
: (6) jumper/lifted lead controls;
: [[RHR]] [[-]]
: (7) test data;
MO-13A following motor pinion inspectionThe inspectors completed three samples. b.FindingsNo findings of significance were identified.1EP2Alert Notification System Testing (71114.02) a.Inspection ScopeThe inspector discussed with licensee staff the status of offsite siren and tone alert radiosystems to determine the adequacy of licensee methods for testing the alert and
: (8) testing frequency and method demonstrated TS operability;
notification system in accordance with 10 CFR  50, Appendix E, "Emergency Planning
: (9) test equipment removal;
and Preparedness."  The inspector observed a monthly siren test on July 24, 2007,
: (10) restoration of plant systems;
performed from the Emergency Operation Facility. The licensee's alert and notification
: (11) fulfillment of American Society Mechanical Engineers Code requirements;
system testing program was compared with criteria in
: (12) engineering evaluations, root causes, and bases for returning tested SSCs not meeting the test acceptance criteria were correct;
: [[NUR]] [[]]
: (13) reference setting data;  and
EG-0654, "Criteria for
: (14) annunciators and alarms setpoints.
Preparation and Evaluation of Radiological Emergency Response Plans and
 
Preparedness in Support of Nuclear Power Plants," Revision 1, Federal Emergency
The inspectors also verified that the licensee identified and implemented any needed corrective actions associated with the surveillance testing.*August 1, 2007, DG Fuel Oil Availability*August 6, 2007, Standby Liquid Control Tank Sample
Management Agency (FEMA) Report REP-10, "Guide for the Evaluation of Alert and
*August 7, 2007, RHR-MO-13A following motor pinion inspectionThe inspectors completed three samples.
Notification Systems for Nuclear Power Plants," and the licensee's current
 
: [[FE]] [[]]
====b. Findings====
MA-approved alert and notification system design report. The inspector also
No findings of significance were identified.1EP2Alert Notification System Testing (71114.02)
reviewed the references listed in the Attachment to this report.
 
Enclosure-12-The inspector completed one sample during the inspection. b.FindingsNo findings of significance were identified.1EP3Emergency Response Organization Augmentation Testing (71114.03) a.Inspection ScopeThe inspector discussed with licensee staff the status of primary and backup systemsfor augmenting the on-shift emergency response staff to determine the adequacy of
====a. Inspection Scope====
licensee methods for staffing emergency response facilities. The inspector reviewed the
The inspector discussed with licensee staff the status of offsite siren and tone alert radiosystems to determine the adequacy of licensee methods for testing the alert and notification system in accordance with 10 CFR  50, Appendix E, "Emergency Planning and Preparedness."  The inspector observed a monthly siren test on July 24, 2007, performed from the Emergency Operation Facility. The licensee's alert and notification system testing program was compared with criteria in NUREG-0654, "Criteria for Preparation and Evaluation of Radiological Emergency Response Plans and Preparedness in Support of Nuclear Power Plants," Revision 1, Federal Emergency Management Agency (FEMA) Report REP-10, "Guide for the Evaluation of Alert and Notification Systems for Nuclear Power Plants," and the licensee's current FEMA-approved alert and notification system design report. The inspector also reviewed the references listed in the Attachment to this report.
references listed in the Attachment to this report related to the emergency response
 
organization (ERO) augmentation system to evaluate the licensee's ability to staff the
-12-The inspector completed one sample during the inspection.
emergency response facilities in accordance with the licensee emergency plan and the
 
requirements of
====b. Findings====
: [[10 CFR]] [[50 Appendix E.The inspector completed one sample during the inspection. b.FindingsNo findings of significance were identified.1]]
No findings of significance were identified.1EP3Emergency Response Organization Augmentation Testing (71114.03)
EP5Correction of Emergency Preparedness Weaknesses and Deficiencies (71114.05) a.Inspection ScopeThe inspector reviewed the licensee's corrective action program (CAP) requirements inAdministrative Procedure 0.5.CR, "Condition Report Initiation, Review, and
 
Classification," Revision 7. The inspector reviewed summaries of approximately 200
====a. Inspection Scope====
condition reports assigned to the emergency planning department during calendar years
The inspector discussed with licensee staff the status of primary and backup systemsfor augmenting the on-shift emergency response staff to determine the adequacy of licensee methods for staffing emergency response facilities. The inspector reviewed the references listed in the Attachment to this report related to the emergency response organization (ERO) augmentation system to evaluate the licensee's ability to staff the emergency response facilities in accordance with the licensee emergency plan and the requirements of 10 CFR 50 Appendix E.The inspector completed one sample during the inspection.
2006 and 2007, and selected 26 for detailed review against the program requirements.
 
The inspector evaluated the response to the corrective action requests to determine the
====b. Findings====
licensee's ability to identify, evaluate, and correct problems in accordance with the
No findings of significance were identified.1EP5Correction of Emergency Preparedness Weaknesses and Deficiencies (71114.05)
licensee program requirements and
 
: [[10 CFR]] [[50.47(b)(14) and 10]]
====a. Inspection Scope====
CFR 50 Appendix
The inspector reviewed the licensee's corrective action program (CAP) requirements inAdministrative Procedure 0.5.CR, "Condition Report Initiation, Review, and Classification," Revision 7. The inspector reviewed summaries of approximately 200 condition reports assigned to the emergency planning department during calendar years 2006 and 2007, and selected 26 for detailed review against the program requirements.
: [[E.]] [[The inspector also reviewed other documents listed in the attachment to this report.The inspector completed one sample during the inspection. b.FindingsNo findings of significance were identified.2.RADIATION]]
 
: [[SAFETY]] [[Cornerstone:  Occupational Radiation Safety []]
The inspector evaluated the response to the corrective action requests to determine the licensee's ability to identify, evaluate, and correct problems in accordance with the licensee program requirements and 10 CFR 50.47(b)(14) and 10 CFR 50 Appendix E.
OS]
 
Enclosure-13-2OS1Access Control To Radiologically Significant Areas (71121.01) a.Inspection ScopeThis area was inspected to assess the licensee's performance in implementing physicaland administrative controls for airborne radioactivity areas, radiation areas, high
The inspector also reviewed other documents listed in the attachment to this report.The inspector completed one sample during the inspection.
radiation areas, and worker adherence to these controls. The inspector used the
 
requirements in 10 CFR Part 20, the technical specifications, and the licensee's
====b. Findings====
procedures required by technical specifications as criteria for determining compliance.
No findings of significance were identified.2.RADIATION SAFETYCornerstone:  Occupational Radiation Safety [OS]
During the inspection, the inspector interviewed the radiation protection manager,
-13-2OS1Access Control To Radiologically Significant Areas (71121.01)
radiation protection supervisors, and radiation workers. The inspector performed
 
independent radiation dose rate measurements and reviewed the following items:*Radiation work permits, procedures, engineering controls, and air samplerlocations*Conformity of electronic personal dosimeter alarm set points with surveyindications and plant policy; workers' knowledge of required actions when their
====a. Inspection Scope====
electronic personnel dosimeter noticeably malfunctions or alarms *Barrier integrity and performance of engineering controls in airborne radioactivityareas*Physical and programmatic controls for highly activated or contaminatedmaterials (non-fuel) stored within spent fuel and other storage pools.  *Self-assessments, audits, licensee event reports, and special reports related tothe access control program since the last inspection*Corrective action documents related to access controls  
This area was inspected to assess the licensee's performance in implementing physicaland administrative controls for airborne radioactivity areas, radiation areas, high radiation areas, and worker adherence to these controls. The inspector used the requirements in 10 CFR Part 20, the technical specifications, and the licensee's procedures required by technical specifications as criteria for determining compliance.
 
During the inspection, the inspector interviewed the radiation protection manager, radiation protection supervisors, and radiation workers. The inspector performed independent radiation dose rate measurements and reviewed the following items:*Radiation work permits, procedures, engineering controls, and air samplerlocations*Conformity of electronic personal dosimeter alarm set points with surveyindications and plant policy; workers' knowledge of required actions when their electronic personnel dosimeter noticeably malfunctions or alarms *Barrier integrity and performance of engineering controls in airborne radioactivityareas*Physical and programmatic controls for highly activated or contaminatedmaterials (non-fuel) stored within spent fuel and other storage pools.  *Self-assessments, audits, licensee event reports, and special reports related tothe access control program since the last inspection*Corrective action documents related to access controls  
*Licensee actions in cases of repetitive deficiencies or significant individualdeficiencies *Radiation work permit briefings and worker instructions  
*Licensee actions in cases of repetitive deficiencies or significant individualdeficiencies *Radiation work permit briefings and worker instructions  
*Adequacy of radiological controls, such as required surveys, radiation protectionjob coverage, and contamination control during job performance *Dosimetry placement in high radiation work areas with significant dose rategradients*Changes in licensee procedural controls of high dose rate - high radiation areasand very high radiation areas*Controls for special areas that have the potential to become very high radiationareas during certain plant operations
*Adequacy of radiological controls, such as required surveys, radiation protectionjob coverage, and contamination control during job performance *Dosimetry placement in high radiation work areas with significant dose rategradients*Changes in licensee procedural controls of high dose rate - high radiation areasand very high radiation areas*Controls for special areas that have the potential to become very high radiationareas during certain plant operations  
Enclosure-14-*Posting and locking of entrances to all accessible high dose rate - high radiationareas and very high radiation areas*Radiation worker and radiation protection technician performance with respect toradiation protection work requirements *Either because the conditions did not exist or an event had not occurred, noopportunities were available to review the following item:*Adequacy of the licensee's internal dose assessment for any actual internalexposure greater than 50 millirem committed effective dose equivalent The inspector completed 18 of the required 21 samples. b.FindingsNo findings of significance were identified.2OS2ALARA Planning and Controls (71121.02) a.Inspection ScopeThe inspector assessed licensee performance with respect to maintaining individual andcollective radiation exposures as low as is reasonably achievable (ALARA). The
-14-*Posting and locking of entrances to all accessible high dose rate - high radiationareas and very high radiation areas*Radiation worker and radiation protection technician performance with respect toradiation protection work requirements *Either because the conditions did not exist or an event had not occurred, noopportunities were available to review the following item:*Adequacy of the licensee's internal dose assessment for any actual internalexposure greater than 50 millirem committed effective dose equivalent The inspector completed 18 of the required 21 samples.
inspector used the requirements in 10 CFR Part 20 and the licensee's procedures
 
required by technical specifications as criteria for determining compliance. The
====b. Findings====
inspector interviewed licensee personnel and reviewed:*Current 3-year rolling average collective exposure
No findings of significance were identified.2OS2ALARA Planning and Controls (71121.02)
*Assumptions and basis for the current annual collective exposure estimate, themethodology for estimating work activity exposures, the intended dose outcome,
 
and the accuracy of dose rate and man-hour estimates*Declared pregnant workers during the current assessment period, monitoringcontrols, and the exposure results*Self-assessments, audits, and special reports related to the
====a. Inspection Scope====
: [[ALA]] [[]]
The inspector assessed licensee performance with respect to maintaining individual andcollective radiation exposures as low as is reasonably achievable (ALARA). The inspector used the requirements in 10 CFR Part 20 and the licensee's procedures required by technical specifications as criteria for determining compliance. The inspector interviewed licensee personnel and reviewed:*Current 3-year rolling average collective exposure
RA programsince the last inspectionDocuments reviewed by inspector included:
*Assumptions and basis for the current annual collective exposure estimate, themethodology for estimating work activity exposures, the intended dose outcome, and the accuracy of dose rate and man-hour estimates*Declared pregnant workers during the current assessment period, monitoringcontrols, and the exposure results*Self-assessments, audits, and special reports related to the ALARA programsince the last inspectionDocuments reviewed by inspector included:
Condition Reports:2007-05267, 2007-05268Procedures*9.ALARA.5ALARA Planning and Controls, Revision 17*9.ALARA.9Dose Determination to the Embryo/Fetus, Revision 0
Condition Reports:2007-05267, 2007-05268Procedures*9.ALARA.5ALARA Planning and Controls, Revision 17*9.ALARA.9Dose Determination to the Embryo/Fetus, Revision 0  
Enclosure-15-The inspector completed 4 of the required 15 samples. b.FindingsNo findings of significance were identified.2PS1Radioactive Gaseous and Liquid Effluent Treatment And Monitoring Systems(71122.01)   a.Inspection ScopeThis area was inspected to ensure that the gaseous and liquid effluent processingsystems are maintained so that radiological releases are properly mitigated, monitored,
-15-The inspector completed 4 of the required 15 samples.
and evaluated with respect to public exposure. The inspector used the requirements in
 
: [[CFR]] [[Part 20, 10]]
====b. Findings====
CFR Part 50 Appendices A and I, the Offsite Dose Calculation
No findings of significance were identified.2PS1Radioactive Gaseous and Liquid Effluent Treatment And Monitoring Systems(71122.01)
Manual, and the licensee's procedures required by technical specifications as criteria fordetermining compliance. The inspector interviewed licensee personnel and reviewed: *Effluent monitoring system modifications
 
Documents reviewed by inspector included:           *NEDC 92-207- Kaman Radiation Monitor Sample Line Plate Out Calculation
====a. Inspection Scope====
*Change Evaluation Document 6015500 - Multi-Purpose Facility Kaman EffluentMonitor Replacement*Drawing Number:
This area was inspected to ensure that the gaseous and liquid effluent processingsystems are maintained so that radiological releases are properly mitigated, monitored, and evaluated with respect to public exposure. The inspector used the requirements in 10 CFR Part 20, 10 CFR Part 50 Appendices A and I, the Offsite Dose Calculation Manual, and the licensee's procedures required by technical specifications as criteria fordetermining compliance. The inspector interviewed licensee personnel and reviewed: *Effluent monitoring system modifications Documents reviewed by inspector included:
: [[SKE]] [[-6015500-01, Revision]]
          *NEDC 92-207- Kaman Radiation Monitor Sample Line Plate Out Calculation
BThe inspector completed 1 of the required 11 samples. b.FindingsIntroduction. The inspector identified a noncited violation of 10 CFR 20.1302(a)because the licensee's surveys of effluents containing radioactive particulates were not
*Change Evaluation Document 6015500 - Multi-Purpose Facility Kaman EffluentMonitor Replacement*Drawing Number: SKE-6015500-01, Revision BThe inspector completed 1 of the required 11 samples.
adequate to ensure compliance with the dose limits for individual members of the public
 
in 10 CFR 20.1301. The violation had very low safety significance.Description. The licensee replaced the instruments used to detect radioactiveparticulates and iodine in the multi-purpose facility ventilation exhaust with sampling
====b. Findings====
filters. The design modification on the effluent monitoring system became operational
 
February 13, 2007. During a walkdown of the sampling system, the inspector noted the
=====Introduction.=====
licensee modified the sampling line configuration through the introduction of a tee in the
The inspector identified a noncited violation of 10 CFR 20.1302(a)because the licensee's surveys of effluents containing radioactive particulates were not adequate to ensure compliance with the dose limits for individual members of the public in 10 CFR 20.1301. The violation had very low safety significance.Description. The licensee replaced the instruments used to detect radioactiveparticulates and iodine in the multi-purpose facility ventilation exhaust with sampling filters. The design modification on the effluent monitoring system became operational February 13, 2007. During a walkdown of the sampling system, the inspector noted the licensee modified the sampling line configuration through the introduction of a tee in the line to allow switching of the air flow to either the A or B sampler. Following interviews and a review of design change documents, the inspector determined the licensee had not reviewed the design changes using the same methodology, from ANSI 13.1 - 1969, "American National Standard Guide to Sampling Airborne Radioactive Materials in Nuclear Facilities," it committed to using when the effluent monitoring instrumentation was originally installed. ANSI 13.1 - 1969 states, "Elbows in sampling lines should be avoided, if at all possible."
line to allow switching of the air flow to either the A or B sampler. Following interviews
 
and a review of design change documents, the inspector determined the licensee had
-16-In response, the licensee documented the problem in the CAP, declared themulti-purpose facility effluent monitoring system inoperable, and performed an apparent cause evaluation. The apparent cause evaluation identified two contributing factors.
not reviewed the design changes using the same methodology, from
 
: [[AN]] [[]]
The design change was "outsourced" and the work request or task agreement contained no instructions the design needed to conform to the ANSI 13.1 - 1969 methodology. Also, the design preparer (vendor) and reviewer (in-house) had the mindset the design was downgraded with less stringent design requirements.The licensee walked down the effluent sampling lines to determine the extent ofcondition and found the remaining sampling lines met the ANSI 13.1 - 1969 guidelines, with the exception of those to the alternate samplers in the turbine, radwaste, and reactor buildings. The alternate samplers also used tee connectors.  (Condition Report 2007-05726, Corrective Action 2 will address the alternate sampler configuration.)Analysis. The licensee made changes to a previously analyzed effluent samplingsystem without updating its analysis to determine the effect on iodine plateout and particle deposition of placing a 90 degree bend in effluent sampling lines. Because the licensee had not followed the ANSI guidance for system analysis nor tested the final configuration to determine the effect on particulate sampling, it could not confirm its sampling results were representative of multi-purpose facility effluent releases. Without representative samples, the licensee could not adequately perform an evaluation or survey. The failure to survey effluents is a performance deficiency. The finding is associated with one of the Public Radiation Safety cornerstone attributes (plant equipment and instrumentation) and affects the associated cornerstone objective, in that the failure to survey effluents for radioactivity could lead to increased public dose. The finding involved an occurrence in the licensee's radiological effluent monitoring program that is contrary to NRC regulations. When processed through the Public Radiation Safety Significance Determination Process, the finding was determined to be of very low safety significance because it:
SI 13.1 - 1969,
: (1) was not a radioactive material control problem, (2)was an effluent release program problem,
"American National Standard Guide to Sampling Airborne Radioactive Materials in
: (3) impaired the licensee's ability to assess dose,
Nuclear Facilities," it committed to using when the effluent monitoring instrumentation
: (4) did not result in a total failure to assess dose because the licensee had other means of assessing the effects of particulate and iodine on public dose, and
was originally installed.
: (5) did not result in public doses that exceeded the values of 10 CFR Part 50, Appendix I, or 10 CFR 20.1301(d). In addition, this finding had cross-cutting aspects in the area of human performance and the component of resources because the licensee did not ensure complete, accurate, and up-to-date design documentation requests and specifications were supplied to outsourced engineering providers. (H.2.(c))Enforcement. Part 20.1302(a) of Title 10 of the Code of Federal Regulations requiresthe licensee make or cause to be made, as appropriate, surveys of radiation levels in unrestricted and controlled areas and radioactive materials in effluents released to unrestricted and controlled areas to demonstrate compliance with the dose limits for individual members of the public in 10 CFR 20.1301. The licensee violated 10 CFR 20.1302(a) when they made surveys of radioactive materials in effluents released to unrestricted areas using samples which could not be verified as representative of the effluent stream. This violation was entered into the licensee's CAP by Condition Reports CR-2007-05726 and CR-2007-05733. Because this violation was determined to be of
: [[AN]] [[]]
-17-very low safety significance and was entered into the licensee's CAP, it is being treatedas a noncited violation, consistent with Section VI.A of the NRC Enforcement Policy:
SI 13.1 - 1969 states, "Elbows in sampling lines should be
NCV 05000298/2007004-01, "Failure to Survey Radioactive Effluents".4.OTHER ACTIVITIES
avoided, if at all possible."
{{a|4OA1}}
Enclosure-16-In response, the licensee documented the problem in the CAP, declared themulti-purpose facility effluent monitoring system inoperable, and performed an apparent
==4OA1 Performance Indicator Verification==
cause evaluation. The apparent cause evaluation identified two contributing factors.
{{IP sample|IP=IP 71151}}
The design change was "outsourced" and the work request or task agreement
 
contained no instructions the design needed to conform to the
====a. Inspection Scope====
: [[AN]] [[]]
Cornerstone:  Emergency PreparednessThe inspector reviewed licensee evaluations for the three emergency preparednesscornerstone performance indicators of Drill and Exercise Performance, ERO Participation, and Alert and Notification System Reliability, for the period July 1, 2006 through June 30, 2007. The definitions and guidance of the Nuclear Energy Institute (NEI) 99-02, "Regulatory Assessment Indicator Guideline," Revisions 3 and 4, and the licensee Performance Indicator Procedure 0-PI-1, "Performance Indicator Program,"
SI 13.1 - 1969
Revision 20, were used to verify the accuracy of the licensee's evaluations for each performance indicator reported during the assessment period. The inspector reviewed a sample of drill and exercise scenarios and licensed operatorsimulator training sessions, notification forms, and attendance and critique records associated with training sessions, drills, and exercises conducted during the verification period. The inspector reviewed selected emergency responder qualification, training, and drill participation records. The inspector reviewed alert and notification system testing procedures, maintenance records, and a 100 percent sample of siren test records. The inspector also reviewed other documents listed in the Attachment to this report. The inspector completed three samples during the inspection.
methodology. Also, the design preparer (vendor) and reviewer (in-house) had the
 
mindset the design was downgraded with less stringent design requirements.The licensee walked down the effluent sampling lines to determine the extent ofcondition and found the remaining sampling lines met the
Cornerstone :  Occupational Radiation SafetyOccupational Exposure Control Effectiveness The inspector reviewed licensee documents from April 1 through June 30, 2007. Thereview included corrective action documentation that identified occurrences in locked high radiation areas (as defined in the licensee's technical specifications), very high radiation areas (as defined in 10 CFR 20.1003), and unplanned personnel exposures (as defined in Nuclear Energy Institute (NEI) 99-02, "Regulatory Assessment Indicator Guideline," Revision 4). Additional records reviewed included ALARA records and whole body counts of selected individual exposures. The inspector interviewed licensee personnel that were accountable for collecting and evaluating the performance indicator data. In addition, the inspector toured plant areas to verify that high radiation, locked high radiation, and very high radiation areas were properly controlled. Performance indicator definitions and guidance contained in NEI 99-02, Revision 4, were used to verify the basis in reporting for each data element.
: [[AN]] [[]]
 
SI 13.1 - 1969 guidelines,
-18-The inspector completed the required sample
with the exception of those to the alternate samplers in the turbine, radwaste, and
: (1) in this cornerstone.
reactor buildings. The alternate samplers also used tee connectors.  (Condition Report
 
2007-05726, Corrective Action 2 will address the alternate sampler configuration.)Analysis. The licensee made changes to a previously analyzed effluent samplingsystem without updating its analysis to determine the effect on iodine plateout and
===Cornerstone:===
particle deposition of placing a 90 degree bend in effluent sampling lines. Because the
Public Radiation SafetyRadiological Effluent Technical Specification/Offsite Dose Calculation Manual Radiological Effluent Occurrences The inspector reviewed licensee documents from April 1 through June 30, 2007.Licensee records reviewed included corrective action documentation that identified occurrences for liquid or gaseous effluent releases that exceeded performance indicator thresholds and those reported to the NRC. The inspector interviewed licensee personnel that were accountable for collecting and evaluating the performance indicator data. Performance indicator definitions and guidance contained in NEI 99-02, Revision 4, were used to verify the basis in reporting for each data element.The inspector completed the required sample
licensee had not followed the
: (1) in this cornerstone.
: [[AN]] [[]]
 
SI guidance for system analysis nor tested the final
====b. Findings====
configuration to determine the effect on particulate sampling, it could not confirm its
No findings of significance were identified.4OA2Problem Identification and Resolution (71152)
sampling results were representative of multi-purpose facility effluent releases. Without
 
representative samples, the licensee could not adequately perform an evaluation or
===.1 Emergency Preparedness Problem Identification and Resolution===
survey. The failure to survey effluents is a performance deficiency. The finding is
 
associated with one of the Public Radiation Safety cornerstone attributes (plant
====a. Inspection Scope====
equipment and instrumentation) and affects the associated cornerstone objective, in that
The inspector selected 26 condition reports for detailed review. The condition reportswere reviewed to ensure that the full extent of the issues were identified, an appropriate evaluation was performed, and appropriate corrective actions were specified and prioritized. The inspector evaluated the condition reports and corrective actions against the requirements of Administrative Procedure 0.5.CR, "Condition Report Initiation, Review, and Classification," Revision 7.
the failure to survey effluents for radioactivity could lead to increased public dose. The
 
finding involved an occurrence in the licensee's radiological effluent monitoring program
====b. Findings and Observations====
that is contrary to NRC regulations. When processed through the Public Radiation
No findings of significance were identified.
Safety Significance Determination Process, the finding was determined to be of very low
 
safety significance because it: (1) was not a radioactive material control problem, (2)
===.2 Access Control and ALARA Planning and Controls===
was an effluent release program problem, (3) impaired the licensee's ability to assess
 
dose, (4) did not result in a total failure to assess dose because the licensee had other
====a. Inspection Scope====
means of assessing the effects of particulate and iodine on public dose, and (5) did not
The inspector evaluated the effectiveness of the licensee's problem identification andresolution process with respect to the following inspection areas:*Access Control to Radiologically Significant Areas (Section 2OS1)*ALARA Planning and Controls (Section 2OS2)  
result in public doses that exceeded the values of 10 CFR Part 50, Appendix I, or 10
-19-
CFR 20.1301(d). In addition, this finding had cross-cutting aspects in the area of human
 
performance and the component of resources because the licensee did not ensure
====b. Findings and Observations====
complete, accurate, and up-to-date design documentation requests and specifications
No findings of significance were identified.
were supplied to outsourced engineering providers. (H.2.(c))Enforcement. Part 20.1302(a) of Title 10 of the Code of Federal Regulations requiresthe licensee make or cause to be made, as appropriate, surveys of radiation levels in
 
unrestricted and controlled areas and radioactive materials in effluents released to
===.3 Selected Issue Follow-up Inspection===
unrestricted and controlled areas to demonstrate compliance with the dose limits for
 
individual members of the public in
====a. Inspection Scope====
: [[10 CFR]] [[20.1301. The licensee violated 10]]
In addition to the routine review, the inspectors selected the issues listed below for amore in-depth review. The inspectors considered the following during the review of the licensee's actions:
CFR
: (1) complete and accurate identification of the problem in a timely manner;
20.1302(a) when they made surveys of radioactive materials in effluents released to
: (2) evaluation and disposition of operability/reportability issues; (3)consideration of extent of condition, generic implications, common cause, and previous occurrences;
unrestricted areas using samples which could not be verified as representative of the
: (4) classification and prioritization of the resolution of the problem; (5)identification of root and contributing causes of the problem;
effluent stream. This violation was entered into the licensee's
: (6) identification of corrective actions; and
: [[CAP]] [[by Condition Reports]]
: (7) completion of corrective actions in a timely manner.  *July 27, 2007, RHR 13D declutch mechanism failure*July 31, 2007, Simulator modeling error
: [[CR]] [[-2007-05726 and]]
CR-2007-05733. Because this violation was determined to be of
Enclosure-17-very low safety significance and was entered into the licensee's
: [[CAP]] [[, it is being treatedas a noncited violation, consistent with Section]]
: [[VI.A]] [[of the NRC Enforcement Policy:]]
: [[NCV]] [[05000298/2007004-01, "Failure to Survey Radioactive Effluents".4.]]
: [[OTHER]] [[]]
: [[ACTIVI]] [[]]
: [[TIES]] [[]]
: [[4OA]] [[1Performance Indicator Verification (71151)    a.Inspection ScopeCornerstone:  Emergency PreparednessThe inspector reviewed licensee evaluations for the three emergency preparednesscornerstone performance indicators of Drill and Exercise Performance,]]
ERO
Participation, and Alert and Notification System Reliability, for the period July 1, 2006
through June 30, 2007. The definitions and guidance of the Nuclear Energy Institute
(NEI) 99-02, "Regulatory Assessment Indicator Guideline," Revisions 3 and 4, and the
licensee Performance Indicator Procedure 0-PI-1, "Performance Indicator Program,"
Revision 20, were used to verify the accuracy of the licensee's evaluations for each
performance indicator reported during the assessment period. The inspector reviewed a sample of drill and exercise scenarios and licensed operatorsimulator training sessions, notification forms, and attendance and critique records
associated with training sessions, drills, and exercises conducted during the verification
period. The inspector reviewed selected emergency responder qualification, training,
and drill participation records. The inspector reviewed alert and notification system
testing procedures, maintenance records, and a 100 percent sample of siren test
records. The inspector also reviewed other documents listed in the Attachment to this
report. The inspector completed three samples during the inspection.
Cornerstone :  Occupational Radiation SafetyOccupational Exposure Control Effectiveness
The inspector reviewed licensee documents from April 1 through June 30, 2007. Thereview included corrective action documentation that identified occurrences in locked
high radiation areas (as defined in the licensee's technical specifications), very high
radiation areas (as defined in 10 CFR 20.1003), and unplanned personnel exposures
(as defined in Nuclear Energy Institute (NEI) 99-02, "Regulatory Assessment Indicator
Guideline," Revision 4). Additional records reviewed included
: [[ALA]] [[]]
RA records and
whole body counts of selected individual exposures. The inspector interviewed licensee
personnel that were accountable for collecting and evaluating the performance indicator
data. In addition, the inspector toured plant areas to verify that high radiation, locked
high radiation, and very high radiation areas were properly controlled. Performance
indicator definitions and guidance contained in NEI 99-02, Revision 4, were used to
verify the basis in reporting for each data element.
Enclosure-18-The inspector completed the required sample (1) in this cornerstone. Cornerstone: Public Radiation SafetyRadiological Effluent Technical Specification/Offsite Dose Calculation Manual Radiological Effluent Occurrences The inspector reviewed licensee documents from April 1 through June 30, 2007.Licensee records reviewed included corrective action documentation that identified
occurrences for liquid or gaseous effluent releases that exceeded performance indicator
thresholds and those reported to the NRC. The inspector interviewed licensee
personnel that were accountable for collecting and evaluating the performance indicator
data. Performance indicator definitions and guidance contained in NEI 99-02, Revision
4, were used to verify the basis in reporting for each data element.The inspector completed the required sample (1) in this cornerstone. b.FindingsNo findings of significance were identified.4OA2Problem Identification and Resolution (71152) .1Emergency Preparedness Problem Identification and Resolution     a.Inspection ScopeThe inspector selected 26 condition reports for detailed review. The condition reportswere reviewed to ensure that the full extent of the issues were identified, an appropriate
evaluation was performed, and appropriate corrective actions were specified and
prioritized. The inspector evaluated the condition reports and corrective actions against
the requirements of Administrative Procedure 0.5.CR, "Condition Report Initiation,
Review, and Classification," Revision 7. b.Findings and ObservationsNo findings of significance were identified. .2Access Control and
: [[ALARA]] [[Planning and Controls     a.Inspection ScopeThe inspector evaluated the effectiveness of the licensee's problem identification andresolution process with respect to the following inspection areas:*Access Control to Radiologically Significant Areas (Section 2]]
OS1)*ALARA Planning and Controls (Section 2OS2)
Enclosure-19-     b.Findings and ObservationsNo findings of significance were identified. .3Selected Issue Follow-up Inspection     a.Inspection ScopeIn addition to the routine review, the inspectors selected the issues listed below for amore in-depth review. The inspectors considered the following during the review of the
licensee's actions: (1) complete and accurate identification of the problem in a timely
manner; (2) evaluation and disposition of operability/reportability issues; (3)
consideration of extent of condition, generic implications, common cause, and previous
occurrences; (4) classification and prioritization of the resolution of the problem; (5)
identification of root and contributing causes of the problem; (6) identification of
corrective actions; and (7) completion of corrective actions in a timely manner.  *July 27, 2007, RHR 13D declutch mechanism failure*July 31, 2007, Simulator modeling error
*August 17, 2007, Flow Erosion in DG2 Service Water PipingDocuments reviewed by inspectors included:
*August 17, 2007, Flow Erosion in DG2 Service Water PipingDocuments reviewed by inspectors included:
*CR-CNS-2007-05070*CR-CNS-2007-03569
*CR-CNS-2007-05070*CR-CNS-2007-03569
*CR-CNS-2007-05624The inspectors completed three samples. b.FindingsIntroduction. The inspectors identified a Green NCV regarding the licensee's failure topromptly identify and correct a condition adverse to quality. Specifically, a degraded
*CR-CNS-2007-05624The inspectors completed three samples.
condition was discovered in the service water supply piping to DG2 but was not
 
evaluated for its effect on the operability of DG2 until prompted by inspectors on
====b. Findings====
August 17, 2007. As a result, additional unavailability time was necessary to repair the
 
degraded condition.Description. On August 16, 2007, during a planned surveillance test of
=====Introduction.=====
: [[DG]] [[2, licenseepersonnel discovered a through-wall leak in the service water supply piping to]]
The inspectors identified a Green NCV regarding the licensee's failure topromptly identify and correct a condition adverse to quality. Specifically, a degraded condition was discovered in the service water supply piping to DG2 but was not evaluated for its effect on the operability of DG2 until prompted by inspectors on August 17, 2007. As a result, additional unavailability time was necessary to repair the degraded condition.Description. On August 16, 2007, during a planned surveillance test of DG2, licenseepersonnel discovered a through-wall leak in the service water supply piping to DG2. As a result of the through-wall leak in the piping, the licensee declared both loops of service water inoperable due to cross-connected nature of the system. Shortly thereafter, the licensee closed a normally open cross connect valve, splitting the two service water loops and restoring the operability of service water loop A. This left DG2 and service water loop B inoperable and the licensee began planning a repair. In preparation for the repair, licensee personnel conducted an ultrasonic survey of thearea surrounding the leak for the purpose of determining the most appropriate repair method. As a precaution, the surrounding piping was also surveyed for indications of
DG2. As
-20-pipe wall thinning. This survey revealed an additional area of pipe that appeared to beless than the minimum wall thickness of 0.111 inches. The estimated thickness at this location was 0.1 inches.This additional indication was discussed during the planning process for the through-wallleak. As documented in CR-CNS-2007-05624, the licensee considered the options available to address the degraded condition of the service water piping in DG2. While there was recognition that an additional degraded condition existed beyond the through-wall leak, the licensee elected not to attempt a repair of this area because the necessary replacement parts had not yet been received. The decision was made to repair only the through-wall leak. This repair was planned and completed by Work Order 4583607 during the night shift on August 16. DG2 was loaded for a post-maintenance test at 0247 on August 17, 2007.Upon reporting to the site on the morning of August 17, the inspectors noted thediscussion in the outage control center logs about the second indication of wall thinning below minimum wall thickness. The inspectors challenged the licensee regarding this additional indication and learned that the condition had not been entered into the CAP, nor had it been evaluated for its impact on the operability of DG2. In response to the inspector's concerns, the licensee conducted an additional ultrasonic survey of the DG2 piping and discovered that the area in question was worn to between 0.06 and 0.08 inch remaining wall thickness, approximately half of minimum wall thickness. Based upon this information, the licensee elected to tag out DG2 again and perform a more extensive internal repair of the eroded service water piping. This repair was completed and service water loop B was declared operable at 2021 on August 17, 2007. DG2 was subsequently declared operable at 2104 on August 17, 2007.The through-wall leak was assumed to be a contemporary manifestation of thepreviously-observed flow erosion in this section of the service water piping caused by high flow velocity. As a result of the historical erosion at this location, the licensee's preventative maintenance program requires an ultrasonic inspection of the piping each operating cycle. The inspectors reviewed the results of the most recent inspection of this location, performed September 17, 2006. The inspectors noted that the ultrasonic test did not reveal the fact that either of the areas that required repair in August 2007 were showing signs of wall thinning in September 2006.The inspectors noted that in response to this event, the licensee has initiated correctiveactions to improve the preventative maintenance tasks for inspecting this section of piping and evaluate the service water system for other areas vulnerable to flow induced erosion. In addition, new materials are being considered for improved resistance to flow induced erosion in this section of piping.Analysis. The performance deficiency associated with this finding involved thelicensee's failure to promptly identify and correct a condition adverse to quality. The finding is more than minor because if left uncorrected, the flow erosion of the DG2 service water supply piping could have become a more significant safety concern.
a result of the through-wall leak in the piping, the licensee declared both loops of service
 
water inoperable due to cross-connected nature of the system. Shortly thereafter, the
Using Inspection Manual Chapter 0609, Appendix A, "Determining the Significance of Reactor Inspection Findings for At-Power Situations," the finding was determined to be  
licensee closed a normally open cross connect valve, splitting the two service water
-21-of very low safety significance because it did not represent an actual loss of safetyfunction of the diesel generator for greater than its technical specification allowed outage time. The cause of this finding is related to the problem identification and resolution cross-cutting component of CAP in that the licensee did not identify and correct the degraded condition of the DG2 service water piping in a timely manner (P.1(a)).Enforcement. 10 CFR 50, Appendix B, Criterion XVI, "Corrective Action," requires, inpart, that measures be established to assure that conditions adverse to quality are promptly identified and corrected. Contrary to this, a degraded condition was discovered in the service water supply piping to DG2 on August 16, 2007, but was not corrected until the licensee was prompted by inspectors on August 17, 2007. As a result, additional unavailability time was necessary to repair the degraded condition.
loops and restoring the operability of service water loop
 
: [[A.]] [[This left]]
Because the finding is of very low safety significance and has been entered into the licensee's CAP as Condition Report CR-CNS-2007-05590, this violation is being treated as an NCV consistent with Section VI.A of the Enforcement Policy:  NCV 05000298/2007004-002, "Failure to Promptly Identify and Correct Flow Erosion in Service Water Piping".4OA3Event Follow-up (71153)
DG2 and service
 
water loop B inoperable and the licensee began planning a repair. In preparation for the repair, licensee personnel conducted an ultrasonic survey of thearea surrounding the leak for the purpose of determining the most appropriate repair
===.1 Failure to Follow Requirements of Industrial Safety Procedures===
method. As a precaution, the surrounding piping was also surveyed for indications of
 
Enclosure-20-pipe wall thinning. This survey revealed an additional area of pipe that appeared to beless than the minimum wall thickness of 0.111 inches. The estimated thickness at this
====a. Inspection Scope====
location was 0.1 inches.This additional indication was discussed during the planning process for the through-wallleak. As documented in
The inspectors reviewed the licensee's response to a toxic gas release on site on July 27, 2007. The inspectors reviewed the licensee's control of the evolution through work control documents, established procedures and operating logs. The followup inspection also reviewed the cause of the release and the licensee's corrective actions.Documents reviewed by inspectors included:
: [[CR]] [[-]]
CNS-2007-05624, the licensee considered the options
available to address the degraded condition of the service water piping in DG2. While
there was recognition that an additional degraded condition existed beyond the
through-wall leak, the licensee elected not to attempt a repair of this area because the
necessary replacement parts had not yet been received. The decision was made to
repair only the through-wall leak. This repair was planned and completed by Work
Order 4583607 during the night shift on August 16. DG2 was loaded for a
post-maintenance test at 0247 on August 17, 2007.Upon reporting to the site on the morning of August 17, the inspectors noted thediscussion in the outage control center logs about the second indication of wall thinning
below minimum wall thickness. The inspectors challenged the licensee regarding this
additional indication and learned that the condition had not been entered into the CAP,
nor had it been evaluated for its impact on the operability of DG2. In response to the
inspector's concerns, the licensee conducted an additional ultrasonic survey of the DG2
piping and discovered that the area in question was worn to between 0.06 and 0.08 inch
remaining wall thickness, approximately half of minimum wall thickness. Based upon
this information, the licensee elected to tag out DG2 again and perform a more
extensive internal repair of the eroded service water piping. This repair was completed
and service water loop B was declared operable at 2021 on August 17, 2007. DG2 was
subsequently declared operable at 2104 on August 17, 2007.The through-wall leak was assumed to be a contemporary manifestation of thepreviously-observed flow erosion in this section of the service water piping caused by
high flow velocity. As a result of the historical erosion at this location, the licensee's
preventative maintenance program requires an ultrasonic inspection of the piping each
operating cycle. The inspectors reviewed the results of the most recent inspection of
this location, performed September 17, 2006. The inspectors noted that the ultrasonic
test did not reveal the fact that either of the areas that required repair in August 2007
were showing signs of wall thinning in September 2006.The inspectors noted that in response to this event, the licensee has initiated correctiveactions to improve the preventative maintenance tasks for inspecting this section of
piping and evaluate the service water system for other areas vulnerable to flow induced
erosion. In addition, new materials are being considered for improved resistance to flow
induced erosion in this section of piping.Analysis. The performance deficiency associated with this finding involved thelicensee's failure to promptly identify and correct a condition adverse to quality. The
finding is more than minor because if left uncorrected, the flow erosion of the DG2
service water supply piping could have become a more significant safety concern.
Using Inspection Manual Chapter 0609, Appendix A, "Determining the Significance of
Reactor Inspection Findings for At-Power Situations," the finding was determined to be
Enclosure-21-of very low safety significance because it did not represent an actual loss of safetyfunction of the diesel generator for greater than its technical specification allowed
outage time. The cause of this finding is related to the problem identification and resolution cross-cutting component of CAP in that the licensee did not identify and correct the degraded
condition of the
: [[DG]] [[2 service water piping in a timely manner (P.1(a)).Enforcement. 10]]
CFR 50, Appendix B, Criterion XVI, "Corrective Action," requires, inpart, that measures be established to assure that conditions adverse to quality are
promptly identified and corrected. Contrary to this, a degraded condition was
discovered in the service water supply piping to DG2 on August 16, 2007, but was not
corrected until the licensee was prompted by inspectors on August 17, 2007. As a
result, additional unavailability time was necessary to repair the degraded condition.
Because the finding is of very low safety significance and has been entered into the
licensee's
: [[CAP]] [[as Condition Report]]
CR-CNS-2007-05590, this violation is being treated
as an
: [[NCV]] [[consistent with Section]]
VI.A of the Enforcement Policy:  NCV
05000298/2007004-002, "Failure to Promptly Identify and Correct Flow Erosion in
Service Water Piping".4OA3Event Follow-up (71153) .1Failure to Follow Requirements of Industrial Safety Procedures       a.Inspection ScopeThe inspectors reviewed the licensee's response to a toxic gas release on site on
July 27, 2007. The inspectors reviewed the licensee's control of the evolution through
work control documents, established procedures and operating logs. The followup
inspection also reviewed the cause of the release and the licensee's corrective actions.Documents reviewed by inspectors included:
*Administrative Procedure 0.36, "Industrial Safety Procedure," Revision 28*Administrative Procedure 0.36.6, "Monitoring for Industrial Gases," Revision 4
*Administrative Procedure 0.36, "Industrial Safety Procedure," Revision 28*Administrative Procedure 0.36.6, "Monitoring for Industrial Gases," Revision 4
*WO 4559451
*WO 4559451
*CR-CNS-2007-05169
*CR-CNS-2007-05169
*CR-CNS-2007-06241     b.FindingsIntroduction. The inspectors identified a Green finding regarding the licensee's failureto follow the requirements of industrial safety procedures. Specifically, licensee
*CR-CNS-2007-06241
personnel violated the requirements of Administrative Procedure 0.36, "Industrial Safety
 
Procedure," and Administrative Procedure 0.36.6, "Monitoring for Industrial Gases,"
====b. Findings====
during a chemical injection treatment in the service water system.Description. On July 27, 2007, the licensee commenced a chemical treatmentprocedure per WO 4559451 in an effort to mitigate previously identified macro-fouling in
 
Enclosure-22-the safety-related service water system. The chemical treatment was being performedby a contractor overseen by station personnel, using a temporary system designed to
=====Introduction.=====
inject high concentrations of chlorine and chlorine dioxide into the service water system.
The inspectors identified a Green finding regarding the licensee's failureto follow the requirements of industrial safety procedures. Specifically, licensee personnel violated the requirements of Administrative Procedure 0.36, "Industrial Safety Procedure," and Administrative Procedure 0.36.6, "Monitoring for Industrial Gases,"
The temporary system included several gaseous concentration monitors designed to
during a chemical injection treatment in the service water system.Description. On July 27, 2007, the licensee commenced a chemical treatmentprocedure per WO 4559451 in an effort to mitigate previously identified macro-fouling in  
warn personnel if potentially dangerous chemical leaks were present.In preparation for this procedure, the supervising engineer prepared a hazardous workpermit (HWP) as required by Administrative Procedure 0.36, "Industrial Safety
-22-the safety-related service water system. The chemical treatment was being performedby a contractor overseen by station personnel, using a temporary system designed to inject high concentrations of chlorine and chlorine dioxide into the service water system.
Procedure," Revision 28. Step 3.33.1 states that:"In order to establish these controls, the HWP should be used to controlconditions, specify necessary engineering controls, compensatory measures, or
 
Personal Protective Equipment (PPE) to be used,
The temporary system included several gaseous concentration monitors designed to warn personnel if potentially dangerous chemical leaks were present.In preparation for this procedure, the supervising engineer prepared a hazardous workpermit (HWP) as required by Administrative Procedure 0.36, "Industrial Safety Procedure," Revision 28. Step 3.33.1 states that:"In order to establish these controls, the HWP should be used to controlconditions, specify necessary engineering controls, compensatory measures, or Personal Protective Equipm ent (PPE) to be used, ...."In addition, step 3.33.4 states that:"The Hazardous Work Permit Supplementary Time Report Form (Attachment 2)serves as the record (i.e. sign in log) for personnel entering an HWP controlled area, provides special instructions, and provides a record..."Contrary to these requirements, the HWP generated for WO 4559451 did not list allchemicals to which maintenance personnel would be exposed. Specifically, the processgenerated chlorine gas, which was not listed in the HWP, and as such personnel were not briefed on the hazards, exposure limits or appropriate PPE. Additionally, the HWP was not maintained at the job site and was not reviewed and signed by the personnel doing the work in the field. As a result, those personnel did not get the full benefit of the safety information and instructions written on the form.In addition, station personnel failed to follow the requirements of Procedure 0.36.6,"Monitoring for Industrial Gases," Revision 4, following receipt of a valid toxic gas alarm in the intake structure on July 29, 2007. During the chemical treatment process, a leak developed in the temporary chlorination piping, resulting in an airborne release of chlorine and chlorine dioxide gases. The locally installed mulit-gas alarm went off and indicated a general area chlorine dioxide concentration at the short term exposure limit of 0.3 ppm for chlorine dioxide. Procedure 0.36.6 provides a warning in section 4 prohibiting entry into a work space if a hazardous atmosphere is indicated. In addition, step 4.5 requires that "if at any time while working within the confined space the monitor alarms, evacuate the work space immediately."  Contrary to these requirements, the maintenance personnel did not exit the space in light of the chlorine dioxide gas alarm.
: [[....]] [["In addition, step 3.33.4 states that:"The Hazardous Work Permit Supplementary Time Report Form (Attachment 2)serves as the record (i.e. sign in log) for personnel entering an]]
 
HWP controlled
Instead, they used the alarming instrument to walk down the piping and look for the leak without donning any PPE, putting themselves at risk of significant personal injury. In addition, had the maintenance personnel become incapacitated, station operators could have been exposed to a toxic gas environment during the conduct or their normal duties or during event response. The failure to follow the station's industrial safety procedures could have affected the availability of systems necessary to mitigate the consequences of an accident, specifically the safety-related portions of the service water system located within the intake structure.
area, provides special instructions, and provides a record..."Contrary to these requirements, the
 
: [[HWP]] [[generated for]]
-23-In response to these concerns from the inspectors, the licensee initiated                   CR-CNS-2007-05169, which resulted in creating a more thorough HWP to be used in future chemical injection efforts. In addition, the licensee initiated CR-CNS-2007-06241 to address the improper response of maintenance personnel to the receipt of toxic gas alarms in the intake structure.Analysis. The performance deficiency associated with this finding involved thelicensee's failure follow the requirements of Procedure 0.36, "Industrial Safety Procedure," and Procedure 0.36.6, "Monitoring for Industrial Gases."  The finding is more than minor because if left uncorrected, it could become a more significant safety concern if not corrected in that failure to follow industrial safety procedures during chlorine dioxide injections could put personnel at significant risk of injury and could have resulted in a larger toxic gas release in the intake structure, inhibiting operators' ability to access safety related equipment to mitigate the consequences of an accident. Using Inspection Manual Chapter 0609, Appendix A, "Determining the Significance of Reactor Inspection Findings for At-Power Situations," the finding was determined to be of very low safety significance because it did not result in a loss of safety function for any mitigating system.The cause of this finding is related to the human performance cross cutting componentof work practices in that licensee personnel did not follow the requirements of industrial safety procedures as required (H.4(b)).Enforcement. No violation of NRC requirements was identified. This finding is identifiedas FIN 05000298/2007004-003, "Failure to Follow Requirements of Industrial Safety Procedures."
WO 4559451 did not list allchemicals to which maintenance personnel would be exposed. Specifically, the processgenerated chlorine gas, which was not listed in the HWP, and as such personnel were
 
not briefed on the hazards, exposure limits or appropriate
===.2 Inadequate Procedural Guidance to Implement Emergency Plan===
: [[PPE.]] [[Additionally, the]]
 
HWP
====a. Inspection Scope====
was not maintained at the job site and was not reviewed and signed by the personnel
The inspectors reviewed the licensee's response to a toxic gas release on site on July 27, 2007. The inspectors reviewed the licensee's control of the evolution through work control documents, established procedures and operating logs. In addition, the inspectors reviewed the event for compliance with the station Emergency Plan. The followup inspection also reviewed the cause of the release and the licensee's corrective actions.Documents reviewed by inspectors included:
doing the work in the field. As a result, those personnel did not get the full benefit of the
*Emergency Plan Implementing Procedure 5.7.1.7, "Classification," Revision 35*CR-CNS-2007-05135
safety information and instructions written on the form.In addition, station personnel failed to follow the requirements of Procedure 0.36.6,"Monitoring for Industrial Gases," Revision 4, following receipt of a valid toxic gas alarm
 
in the intake structure on July 29, 2007. During the chemical treatment process, a leak
====b. Findings====
developed in the temporary chlorination piping, resulting in an airborne release of
 
chlorine and chlorine dioxide gases. The locally installed mulit-gas alarm went off and
=====Introduction.=====
indicated a general area chlorine dioxide concentration at the short term exposure limit
The inspectors identified a Green NCV regarding the licensee's failure toestablish adequate procedural guidance to implement the emergency plan.
of 0.3 ppm for chlorine dioxide. Procedure 0.36.6 provides a warning in section 4
 
prohibiting entry into a work space if a hazardous atmosphere is indicated. In addition,
-24-Description. On July 27, 2007, the licensee commenced a chemical treatmentprocedure in an effort to mitigate previously identified macro-fouling in the safety-related service water system. The chemical treatment was being performed by a contractor using a temporary system designed to inject high concentrations of chlorine and chlorine dioxide into the service water system. The temporary system included several gaseous concentration monitors designed to warn personnel if potentially dangerous chemical leaks were present.During the treatment on July 29, 2007, a local gaseous concentration alarm went off,warning personnel that chlorine and chlorine dioxide gas were leaking into the intake structure. The maximum general area concentrations recorded by the instrument were 0.3 ppm chlorine dioxide and 0.3 ppm chlorine. The temporary system was immediately secured and the source of the leak was found. This information was reported to control room operators, who determined that the gaseous leak did not meet the entry criteria for any emergency action levels (EALs) listed in Emergency Plan Implementing Procedure 5.7.1, "Emergency Classification." (EPIP 5.7.1). EPIP 5.7.1, Revision 35, Attachment 2 provided the following guidance for classifying toxic gas release events:
step 4.5 requires that "if at any time while working within the confined space the monitor
EALClassificationText                                                                                    5.1.2NOUEReport or detection of toxic or flammable gas that couldenter the Protected Area in amounts that will affect the health of plant personnel or can affect normal plant operations.5.2.2ALERTReport or detection of toxic or flammable gas within a VitalArea in concentrations that will be life threatening to plant personnel or will affect the safe operation of the plant.The inspectors noted that additional information was provided in EPIP 5.7.1 to clarify theentry criterion for EAL 5.2.2. Specifically, the EPIP page for EAL 5.2.2 contained the following additional guidance:  "IDLH atmospheres (for Toxic gases)...in Vital Areas should be considered as meeting this condition."  The inspectors noted that no such clarifying guidance was provided for EAL 5.1.2.The inspectors reviewed the operating logs and discussed the event with operations andemergency planning staff to gain an understanding of the information available to the operators and the rationale used in implementing the emergency plan. The inspectors noted that the operators justified not declaring an event by comparing the immediately dangerous to life or health (IDLH) limits for the toxic gases to the highest concentrations seen in the field. The inspectors determined that this was an appropriate threshold for EAL 5.2.2, but challenged the licensee's treatment of EAL 5.1.2 given the lower threshold described in the EAL 5.1.2 text.Concentrations limits below IDLH have been defined by the Occupational Safety andHealth Administration (OSHA) and National Institute for Occupational Safety and Health(NIOSH). OSHA and NIOSH define the short-term exposure limits (STEL) of 0.3 ppm for chlorine dioxide and 0.5 ppm for chlorine (for comparison, the IDLH concentrations for these gases are 5 ppm for chlorine dioxide and for 10 ppm chlorine). The NIOSH
alarms, evacuate the work space immediately."  Contrary to these requirements, the
-25-standard states that exposures above the STEL concentrations should not exceedfifteen minutes based on the risk of severe respiratory and eye irritation.The inspectors determined that this represented a technical inadequacy in EPIP 5.7.1,in that no specific entry criteria were defined in the EPIP to allow the Emergency Director to determine whether or not toxic gas concentrations were present in "amounts that will affect the health of plant personnel" as described in the EAL 5.1.2 text. This procedural weakness was demonstrated on July 29, 2007, when the concentration of chlorine and chlorine dioxide gas were compared only to IDLH limits during the event classification process. In response to this issue, on August 30, 2007, the licensee revised EPIP 5.7.1 to provide clarification on the entry criteria for EALs 5.1.2 and 5.2.2.
maintenance personnel did not exit the space in light of the chlorine dioxide gas alarm.
 
Instead, they used the alarming instrument to walk down the piping and look for the leak
In addition, the licensee created a required reading task for all control room operators to ensure they understood the technical issue and the new guidance.Based on a review of information collected by the licensee and interviews with personnelwho were present at the time of the chemical leak, the inspectors concluded that on July 29, 2007, the gas monitor being used to detect toxic gas conditions alarmed and indicated that the concentration of chlorine dioxide gas in the intake structure had reached the STEL limit of 0.3 ppm. The leak was immediately secured, after which the monitor was used to locate the specific source of the leak. Chlorine dioxide levels as high as 1.0 ppm were identified during the search for the leak. The licensee has determined that using the new guidance in EPIP 5.7.1, this event would not have resulted in an entry into EAL 5.1.2 due to the fact that the gas monitor was taking a suction approximately eight inches above the floor level and was not representative of the breathing zone to which personnel were exposed.The inspectors reviewed the revision history for EPIP 5.7.1, and noted that periodicreview conducted as required by Administrative Procedure 0.4A,"Procedure Change Process Supplement", Revision 14, did not identify this error. Specifically, the person completing the required periodic review on November 14, 2005, errantly determined that a review of the entire EPIP was not required, and as such missed an opportunity to identify this procedural shortcoming.Analysis. The performance deficiency associated with this finding involved thelicensee's failure to maintain adequate procedural guidance to implement the emergency plan. The finding is more than minor because it is associated with the Emergency Preparedness cornerstone attribute of procedural quality and affects the associated cornerstone objective to ensure that the licensee is capable of implementing adequate measures to protect the health and safety of the public in the event of a radiological emergency. Using Inspection Manual Chapter 0609, Appendix B, "Emergency Preparedness Significance Determination Process," the finding was determined to be of very low safety significance since the EAL classification process that was in place prior to August 30, 2007, could have resulted in a failure to declare a Notification of Unusual Event when it should have been declared. The cause of this finding is related to the human performance cross cutting componentof resources in that complete and accurate procedures were not adequately maintained to support the emergency plan (H.2(c)).  
without donning any PPE, putting themselves at risk of significant personal injury. In
-26-Enforcement. 10 CFR 50.47 (b)(4) requires, in part, that a standard emergencyclassification and action level scheme is in use by the nuclear facility licensee. Contrary to this, Emergency Plan Implementing Procedure 5.7.1, "Emergency Classification",
addition, had the maintenance personnel become incapacitated, station operators could
Revision 35, contained inadequate procedural guidance in that it did not identify any specific entry criteria for Emergency Action Level 5.1.2. As a result, the conditions requiring entry into Emergency Action Level 5.1.2 could have existed without the proper event classification being made. Because the finding is of very low safety significance and has been entered into the licensee's CAP as Condition Report CR-CNS-2007-05135, this violation is being treated as an NCV consistent with Section VI.A of the Enforcement Policy: NCV 05000298/2007004-004, "Inadequate Procedural Guidance to Implement the Emergency Plan"..3(Closed) LER 50-298/2007-004:  Manual Reactor Trip due to Hydraulic Control UnitValve Bonnet Leak into Reactor BuildingOn May 19, 2007, during disassembly of a directional control valve on a control rod drivesystem hydraulic control unit, a water leak developed. Control room operators inserted a manual reactor scram when the leak changed from water to steam and was unable to be isolated. The cause of the leak was a combination of a degraded condition in an upstream isolation valve and a failure by the licensee to implement vendor guidance in isolating the hydraulic control unit for maintenance. This event and the ensuing violation of NRC requirements are discussed in detail in NRC Integrated Inspection Report 05000298/2007003. This LER is closed.4OA6Meetings, Including ExitOn July 26, 2007, a regional inspector conducted an exit meeting to present the resultsof the emergency preparedness program inspection to Mr. M. Colomb, General Manager, Plant Operations. The inspector confirmed that proprietary information was not provided or examined during the inspection.On August 24, 2007, a regional inspector presented the occupational radiation safetyinspection results to Mr. M. Colomb, General Manager, Plant Operations and other members of his staff who acknowledged the findings. The inspector confirmed that proprietary information was not provided or examined during the inspection.On October 4, 2007, the resident inspectors conducted an exit meeting to present theresults of the emergency preparedness program inspection to Mr. M. Colomb, General Manager, Plant Operations and other members of his staff who acknowledged the findings. The inspector confirmed that proprietary information was not provided or examined during the inspection.ATTACHMENT:
have been exposed to a toxic gas environment during the conduct or their normal duties
 
or during event response. The failure to follow the station's industrial safety procedures
=SUPPLEMENTAL INFORMATION=
could have affected the availability of systems necessary to mitigate the consequences
 
of an accident, specifically the safety-related portions of the service water system
==KEY POINTS OF CONTACT==
located within the intake structure.
 
Enclosure-23-In response to these concerns from the inspectors, the licensee initiated
===Licensee Personnel===
: [[CR]] [[-]]
: [[contact::A. Alexander]], Emergency Planning Specialist
CNS-2007-05169, which resulted in creating a more thorough HWP to be used in
: [[contact::T. Bahensky]], System Engineer
future chemical injection efforts. In addition, the licensee initiated
: [[contact::J. Bebb]], Security Manager
: [[CR]] [[-]]
: [[contact::J. Bednar]], Staff Health Physicist, Radiation Protection
CNS-2007-06241
: [[contact::R. Beilke]], Chemistry Manager
to address the improper response of maintenance personnel to the receipt of toxic gas
: [[contact::V. Bhardwaj]], Engineering Support Manager
alarms in the intake structure.Analysis. The performance deficiency associated with this finding involved thelicensee's failure follow the requirements of Procedure 0.36, "Industrial Safety
: [[contact::D. Buman]], Systems Engineering Manager
Procedure," and Procedure 0.36.6, "Monitoring for Industrial Gases."  The finding is
: [[contact::T. Carson]], Maintenance Manager
more than minor because if left uncorrected, it could become a more significant safety
: [[contact::J. Christensen]], Support General Manager
concern if not corrected in that failure to follow industrial safety procedures during
: [[contact::M. Colomb]], Plant Operations General Manager
chlorine dioxide injections could put personnel at significant risk of injury and could have
: [[contact::R. Dyer]], Heat Exchanger Program Engineer
resulted in a larger toxic gas release in the intake structure, inhibiting operators' ability to
: [[contact::J. Dykstra]], Electrical Engineering Program Supervisor
access safety related equipment to mitigate the consequences of an accident. Using
: [[contact::T. Erickson]], System Engineering Supervisor
Inspection Manual Chapter 0609, Appendix A, "Determining the Significance of Reactor
: [[contact::R. Estrada]], Corrective Action Program Manager
Inspection Findings for At-Power Situations," the finding was determined to be of very
: [[contact::K. Fike]], Plant Chemist, Chemistry
low safety significance because it did not result in a loss of safety function for any
: [[contact::J. Flaherty]], Senior Licensing Engineer
mitigating system.The cause of this finding is related to the human performance cross cutting componentof work practices in that licensee personnel did not follow the requirements of industrial
: [[contact::P. Fleming]], Nuclear Safety Assurance Director
safety procedures as required (H.4(b)).Enforcement. No violation of
: [[contact::K. Garner]], Radiological Operations Supervisor, Radiation Protection
: [[NRC]] [[requirements was identified. This finding is identifiedas]]
: [[contact::T. Haynes]], Emergency Planning Specialist
FIN 05000298/2007004-003, "Failure to Follow Requirements of Industrial Safety
: [[contact::T. Hottovy]], Equipment Reliability Supervisor
Procedures." .2Inadequate Procedural Guidance to Implement Emergency Plan       a.Inspection ScopeThe inspectors reviewed the licensee's response to a toxic gas release on site on
: [[contact::T. Hough]], Maintenance Rule Coordinator
July 27, 2007. The inspectors reviewed the licensee's control of the evolution through
: [[contact::J. Kelsay]], Emergency Planning Specialist
work control documents, established procedures and operating logs. In addition, the
: [[contact::G. Kline]], Engineering Director
inspectors reviewed the event for compliance with the station Emergency Plan. The
: [[contact::D. Madsen]], Licensing Specialist
followup inspection also reviewed the cause of the release and the licensee's corrective
: [[contact::M. McCormack]], Electrical Systems/I&C System Engineering Supervisor
actions.Documents reviewed by inspectors included:
: [[contact::E. McCutchen]], Regulatory Affairs Senior Licensing Engineer
*Emergency Plan Implementing Procedure 5.7.1.7, "Classification," Revision 35*CR-CNS-2007-05135     b.Findings   Introduction. The inspectors identified a Green NCV regarding the licensee's failure toestablish adequate procedural guidance to implement the emergency plan.
: [[contact::M. Metzger]], System Engineer
Enclosure-24-Description. On July 27, 2007, the licensee commenced a chemical treatmentprocedure in an effort to mitigate previously identified macro-fouling in the safety-related
: [[contact::S. Minahan]], Vice President - Nuclear & Chief Nuclear Officer
service water system. The chemical treatment was being performed by a contractor
: [[contact::B. Murphy]], Emergency Planning Manager
using a temporary system designed to inject high concentrations of chlorine and chlorine
: [[contact::R. Noon]], Root Cause Team Leader, Corrective Actions
dioxide into the service water system. The temporary system included several gaseous
: [[contact::D. Oshlo]], Radiation Protection Manager
concentration monitors designed to warn personnel if potentially dangerous chemical
: [[contact::S. Rezab]], Emergency Planning Specialist
leaks were present.During the treatment on July 29, 2007, a local gaseous concentration alarm went off,warning personnel that chlorine and chlorine dioxide gas were leaking into the intake
: [[contact::T. Rients]], Emergency Planning Specialist
structure. The maximum general area concentrations recorded by the instrument were
: [[contact::A. Sarver]], Balance of Plant Engineering Supervisor
0.3 ppm chlorine dioxide and 0.3 ppm chlorine. The temporary system was immediately
: [[contact::T. Shudak]], Fire Protection Program Engineer
secured and the source of the leak was found. This information was reported to control
: [[contact::T. Stevens]], Design Engineering Manager
room operators, who determined that the gaseous leak did not meet the entry criteria for
: [[contact::K. Thomas]], Mechanical Programs Supervisor
any emergency action levels (EALs) listed in Emergency Plan Implementing Procedure
: [[contact::J. Waid]], Training Manager
5.7.1, "Emergency Classification." (EPIP 5.7.1).
: [[contact::D. Willis]], Operations Manager
: [[EP]] [[]]
AttachmentA-2
IP 5.7.1, Revision 35, Attachment 2
==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==
provided the following guidance for classifying toxic gas release events:EALClassificationText                                                                                    5.1.2NOUEReport or detection of toxic or flammable gas that couldenter the Protected Area in amounts that will affect the
Opened and
health of plant personnel or can affect normal plant
===Closed===
operations.5.2.2ALERTReport or detection of toxic or flammable gas within a VitalArea in concentrations that will be life threatening to plant
: 05000298/2007-001NCVFailure to Survey Radioactive Effluents05000298/2007-002NCVFailure to Promptly Identify and Correct FlowErosion in Service Water Piping05000298/2007-003FINFailure to Follow Requirements of Industrial SafetyProcedures05000298/2007-004NCVInadequate Procedural Guidance to Implement theEmergency Plan
personnel or will affect the safe operation of the plant.The inspectors noted that additional information was provided in
 
: [[EPIP]] [[5.7.1 to clarify theentry criterion for]]
===Closed===
: [[EAL]] [[5.2.2. Specifically, the]]
: 05000298/2007-001NCVFailure to Survey Radioactive Effluents05000298/2007-002NCVFailure to Promptly Identify and Correct FlowErosion in Service Water Piping05000298/2007-003FINFailure to Follow Requirements of Industrial SafetyProcedures05000298/2007-004NCVInadequate Procedural Guidance to Implement theEmergency Plan
: [[EPIP]] [[page for]]
 
EAL 5.2.2 contained the
==LIST OF DOCUMENTS REVIEWED==
following additional guidance:  "IDLH atmospheres (for Toxic gases)...in Vital Areas should be considered as meeting this condition."  The inspectors noted that no such
Section 1R04 Equipment Alignments (71111.04) Procedures
clarifying guidance was provided for EAL 5.1.2.The inspectors reviewed the operating logs and discussed the event with operations andemergency planning staff to gain an understanding of the information available to the
:NumberDescription
operators and the rationale used in implementing the emergency plan. The inspectors
: RevisionProcedure 5.8.8Alternate Boron Injection 7with RCICSystem Operating Procedure 2.2.67Reactor Core Isolation Cooling System57
noted that the operators justified not declaring an event by comparing the immediately
: System Operating Procedure 2.2.67AReactor Core Isolation Cooling System 19Component ChecklistSystem Operating Procedure 2.2.67BReactor Core Isolation Cooling System1Instrument Valve ChecklistCNS System Health ReportReactor Core Isolation Cooling
dangerous to life or health (IDLH) limits for the toxic gases to the highest concentrations
: June 2007System
seen in the field. The inspectors determined that this was an appropriate threshold for
: June 2007System Operating Procedure 2.2.47A
: [[EAL]] [[5.2.2, but challenged the licensee's treatment of]]
: HVAC Reactor Building Component 14Checklist AttachmentA-3System Operating Procedure 2.2.47HVAC Reactor Building41System Operating Procedure 2.2.47BHVAC Reactor Building Instrument4 Valve ChecklistFSAR/USARUSAR, Volume II, Section IV - 7; Reactor Core Isolation Cooling SystemUSAR, Volume IV, Section X-10, Heating, Ventilation and Air Conditioning Systems
EAL 5.1.2 given the lower
: CNS System Heath Report; Heating and Ventilation reactor Building; June 2007Drawings and DiagramsBR 2043; Reactor Core Isolation Cooling and Reactor Feed System; Revision N49BR 2020; Reactor Building Heating and Ventilation; Revision N56Corrective Action DocumentsCR-CNS-2007-06443Section 1R19 Postmaintenance Testing (71111.19)Procedures:NumberDescription
threshold described in the
: RevisionMaintenance Procedure 7.0.8.1System Leakage Testing21Chemistry Procedure 8.4.1.1Post-Accident Sampling System16
: [[EAL]] [[5.1.2 text.Concentrations limits below]]
: Chemistry Procedure 8.PAA.4Semi-Annual QC and training for6Post-Accident Sampling SystemSurveillance Procedure RHR Power Operated Valve Operability Test206.1RHR.201(IST) (DIV I)Surveillance Procedure Position Indicator Inservice training (IST)136.MISC.401Maintenance Procedure 7.2.30Service Water Zurn Strainer Maintenance9
: [[IDLH]] [[have been defined by the Occupational Safety andHealth Administration (OSHA) and National Institute for Occupational Safety and Health(NIOSH).]]
: WORK ORDERS
: [[OSHA]] [[and]]
:445795244995974535990
NIOSH define the short-term exposure limits (STEL) of 0.3 ppm for
: 449959544995984501093
chlorine dioxide and 0.5 ppm for chlorine (for comparison, the
: 449959644579534583607
: [[ID]] [[]]
: 4585698
LH concentrations for
: AttachmentA-4CONDITION REPORTS
these gases are 5 ppm for chlorine dioxide and for 10 ppm chlorine). The
:CR-CNS-2007-5915SP 6.1
: [[NIO]] [[]]
: DG.401 completed 8/30/2007CR-CNS-2007-5916SP 6.1
: [[SH]] [[Enclosure-25-standard states that exposures above the]]
: DG.301 completed 8/31/2007
: [[STEL]] [[concentrations should not exceedfifteen minutes based on the risk of severe respiratory and eye irritation.The inspectors determined that this represented a technical inadequacy in]]
: CR-CNS-2007-5923
: [[EPIP]] [[5.7.1,in that no specific entry criteria were defined in the]]
: CR-CNS-2007-5929Section 1R22 Surveillance Testi ng (71111.22)Procedures
: [[EP]] [[]]
:NumberDescriptionRevisionSurveillance Procedure 6.SLC.601SLC Tank Sampling7
IP to allow the Emergency
: Chemistry Procedure 8.7.1.4Boron Potentiometric Analysis 11(High Range)Surveillance Procedure 6.DG.601DG Fuel Oil Availability14NEDC 97-012Emergency Diesel Generator Fuel 2Oil On-Site Storage Technical Specification RequirementsSurveillance Procedure 6.1RHR.201RHR Power Operated Valve 20Operability test (IST) (DIV 1)Surveillance Procedure 6.MISC.401Position Indicator Inservice 13Testing (IST)Work Orders:4555054, 4535900Section 1EP2 Alert Notification System Testing (711114.02)Emergency Plan Implementing Procedures (EPIP)5.7.21, "Maintaining Emergency Preparedness -Emergency Exercise, Drills, Tests, andEvaluations," Revision 35
Director to determine whether or not toxic gas concentrations were present in "amounts
: 5.7.21.1, "NOAA/EAS Radio Malfunction," Revision 9
that will affect the health of plant personnel" as described in the EAL 5.1.2 text. This
: 5.7.27, "Alert and Notification System," Revision 17Administrative Procedure O-EP-02, "Configuration Control of the Automated NotificationSystem (ANS)," Revision 4
procedural weakness was demonstrated on July 29, 2007, when the concentration of
: AttachmentA-5Alert and Notification System Design Report, Revision 12, May 2004Section 1EP3 (Emergency Response Organization Augmentation Testing (711114.03)Results of bi-monthly off-hours ERO call-in drills from 3rd quarter 2005 through 2nd quarter2007, and call-out drill conducted on August 22, 2006.Emergency Plan Implementing Procedures (EPIP)5.7, "Communications," Revision 85.7.2, "Emergency Director Emergency Plan Implementing Procedure," Revision 25
chlorine and chlorine dioxide gas were compared only to
: 5.7.25, "Recovery Operations," Revision 16Preventive Measure Test Procedure, "Windows XP Communicator/ Version 9.3 SystemUpgrade," December 27, 2006Section 1EP5 Correction of Emergency Preparedness Weaknesses and Deficiencies(71114.05)Snapshot Assessment/Benchmark on the Entergy Emergency Preparedness DepartmentDuties and Responsibilities, November 21, 2006.Emergency Planning Department On-going Quarterly Assessment Reports, third quarter 2005through first quarter 2007Quality Assurance Audit Report 06-03, "Emergency Planning," March 13-20, 2006
: [[ID]] [[]]
: Quality Assurance Audit Report 07-03, "Emergency Planning," March 12-29, 2007
LH limits during the event
: Apparent Cause Evaluation CR-CNS-2006-10569
classification process. In response to this issue, on August 30, 2007, the licensee
: Root Cause Report, "NOUE Declared in Response to Unverified Fire Alarm," August 24, 2006
revised
===Operating Experience===
: [[EPIP]] [[5.7.1 to provide clarification on the entry criteria for]]
: Report 23107, "March 1, 2006, Susquehanna Alert, Halon in Vital Area" Operating Procedure 5.4, "Fire," Revisions 13, 14
EALs 5.1.2 and 5.2.2.
: Administrative Procedure O.39, "Fire Watches," Revision 34
In addition, the licensee created a required reading task for all control room operators to
 
ensure they understood the technical issue and the new guidance.Based on a review of information collected by the licensee and interviews with personnelwho were present at the time of the chemical leak, the inspectors concluded that on
==Section 2OS1: Access Controls to Radiologically Significant Areas (71121.01) Corrective Action Documents2007-04340, 2007-4933, 2007-05172, 2007-05201, 2007-05297==
July 29, 2007, the gas monitor being used to detect toxic gas conditions alarmed and
: AttachmentA-6Audits and Self-AssessmentsQAD 20070051Quality Assurance Surveillance Report, "Control of Radiological Work"QAD 20070053Quality Assurance Surveillance Report, "Source Term Reduction andControl" Radiological Department On-Going Assessment Report 1Q2007Radiation Work Permits (or Radiation exposure permit)Procedures9.RADOP.3Area Posting and Access Control, Revision 25
indicated that the concentration of chlorine dioxide gas in the intake structure had
: Survey RecordsCNS
reached the
: RP-121Reactor Building - 881' Quads - 6/16/07, 3/06/07, 12/27/06, 9/23/06
: [[ST]] [[]]
: MiscellaneousCNS
EL limit of 0.3 ppm. The leak was immediately secured, after which the
: RP-11High Radiation Area Gate Key Inventory - 6/29/07, 3/29/07CNS
monitor was used to locate the specific source of the leak. Chlorine dioxide levels as
: RP-39Alarming Dosimeter Set Point FormSection 4OA1 Performance Indicator Verification (71151)Semi-monthly siren test results from July 2006 through June 2007Current training records for 10 designated ERO members List of qualified ERO members and positions assigned Critique Reports for Drills and Exercises:Team Evaluated Exercises, July 19 and December 20, 2006Team Evaluated Exercises, March 18, May 16, and July 19, 2007
high as 1.0 ppm were identified during the search for the leak. The licensee has
: Operations Crew Simulator Drills, January through June 2007Critique Reports for Declared Events:Notice of Unusual Event, July 25, 2006 and Event Report 42728Notice of Unusual Event, November 11, 2006 and Event Report 42985Emergency Plan Implementing Procedures (EPIP)5.7.1, "Emergency Classification," Revision 355.7.6, "Notification," Revision 43
determined that using the new guidance in
: AttachmentA-75.7.20, "Protective Action Recommendations," Revision 18Emergency Planning Department Guides#2, Attachment G-1, "Emergency Planning Performance Indicator Guide," Revision 12H1, "CNS Drill and Exercise Manual"Section 4OA2 Problem Identification and Resolution (71152)Cooper Nuclear Station Emergency Plan, Revisions 30, 52Cooper Nuclear Station Emergency Action Levels, Revisions 21, 35
: [[EP]] [[]]
: Condition Reports:
IP 5.7.1, this event would not have
: CR-CNS-
resulted in an entry into EAL 5.1.2 due to the fact that the gas monitor was taking a
: 2006-2416, 2437, 2439, 4508, 5167, 5302, 5303, 5685, 5686, 5722, 5934, 7168, 7222, 7523,10569.
suction approximately eight inches above the floor level and was not representative of
: 2007- 0071, 0993, 1041, 1886, 2142, 2150, 2237, 2352, 2353, 3562, 4398 
the breathing zone to which personnel were exposed.The inspectors reviewed the revision history for
: AttachmentA-8
: [[EP]] [[]]
==LIST OF ACRONYMS==
IP 5.7.1, and noted that periodicreview conducted as required by Administrative Procedure 0.4A,"Procedure Change
ALARAas low as reasonably achievableCAPcorrective action program
Process Supplement", Revision 14, did not identify this error. Specifically, the person
CFRCode of Federal Regulations
completing the required periodic review on November 14, 2005, errantly determined that
a review of the entire
: [[EP]] [[]]
IP was not required, and as such missed an opportunity to
identify this procedural shortcoming.Analysis. The performance deficiency associated with this finding involved thelicensee's failure to maintain adequate procedural guidance to implement the
emergency plan. The finding is more than minor because it is associated with the
Emergency Preparedness cornerstone attribute of procedural quality and affects the
associated cornerstone objective to ensure that the licensee is capable of implementing
adequate measures to protect the health and safety of the public in the event of a
radiological emergency. Using Inspection Manual Chapter 0609, Appendix B,
"Emergency Preparedness Significance Determination Process," the finding was
determined to be of very low safety significance since the EAL classification process
that was in place prior to August 30, 2007, could have resulted in a failure to declare a
Notification of Unusual Event when it should have been declared. The cause of this finding is related to the human performance cross cutting componentof resources in that complete and accurate procedures were not adequately maintained
to support the emergency plan (H.2(c)).
Enclosure-26-Enforcement. 10 CFR 50.47 (b)(4) requires, in part, that a standard emergencyclassification and action level scheme is in use by the nuclear facility licensee. Contrary
to this, Emergency Plan Implementing Procedure 5.7.1, "Emergency Classification",
Revision 35, contained inadequate procedural guidance in that it did not identify any
specific entry criteria for Emergency Action Level 5.1.2. As a result, the conditions
requiring entry into Emergency Action Level 5.1.2 could have existed without the proper
event classification being made. Because the finding is of very low safety significance
and has been entered into the licensee's
: [[CAP]] [[as Condition Report]]
: [[CR]] [[-]]
: [[CNS]] [[-2007-05135, this violation is being treated as an NCV consistent with Section]]
: [[VI.A]] [[of the Enforcement Policy:]]
NCV 05000298/2007004-004, "Inadequate Procedural
Guidance to Implement the Emergency Plan"..3(Closed) LER 50-298/2007-004:  Manual Reactor Trip due to Hydraulic Control UnitValve Bonnet Leak into Reactor BuildingOn May 19, 2007, during disassembly of a directional control valve on a control rod drivesystem hydraulic control unit, a water leak developed. Control room operators inserted
a manual reactor scram when the leak changed from water to steam and was unable to
be isolated. The cause of the leak was a combination of a degraded condition in an
upstream isolation valve and a failure by the licensee to implement vendor guidance in
isolating the hydraulic control unit for maintenance. This event and the ensuing violation
of
: [[NRC]] [[requirements are discussed in detail in]]
NRC Integrated Inspection Report
05000298/2007003. This
: [[LER]] [[is closed.4]]
OA6Meetings, Including ExitOn July 26, 2007, a regional inspector conducted an exit meeting to present the resultsof the emergency preparedness program inspection to Mr. M. Colomb, General
Manager, Plant Operations. The inspector confirmed that proprietary information was
not provided or examined during the inspection.On August 24, 2007, a regional inspector presented the occupational radiation safetyinspection results to Mr. M. Colomb, General Manager, Plant Operations and other
members of his staff who acknowledged the findings. The inspector confirmed that
proprietary information was not provided or examined during the inspection.On October 4, 2007, the resident inspectors conducted an exit meeting to present theresults of the emergency preparedness program inspection to Mr. M. Colomb, General
Manager, Plant Operations and other members of his staff who acknowledged the
findings. The inspector confirmed that proprietary information was not provided or
examined during the inspection.ATTACHMENT:
: [[SUPPLE]] [[]]
: [[MENTAL]] [[]]
: [[INFORM]] [[]]
: [[ATION]] [[AttachmentA-1SUPPLEMENTAL]]
: [[INFORM]] [[]]
: [[ATION]] [[]]
: [[KEY]] [[]]
: [[POINTS]] [[]]
: [[OF]] [[]]
CONTACTLicensee PersonnelA. Alexander, Emergency Planning SpecialistT. Bahensky, System Engineer
J. Bebb, Security Manager
J. Bednar, Staff Health Physicist, Radiation Protection
R. Beilke, Chemistry Manager
V. Bhardwaj, Engineering Support Manager
D. Buman, Systems Engineering Manager
T. Carson, Maintenance Manager
J. Christensen, Support General Manager
M. Colomb, Plant Operations General Manager
R. Dyer, Heat Exchanger Program Engineer
J. Dykstra, Electrical Engineering Program Supervisor
T. Erickson, System Engineering Supervisor
R. Estrada, Corrective Action Program Manager
K. Fike, Plant Chemist, Chemistry
J. Flaherty, Senior Licensing Engineer
P. Fleming, Nuclear Safety Assurance Director
K. Garner, Radiological Operations Supervisor, Radiation ProtectionT. Haynes, Emergency Planning Specialist
T. Hottovy, Equipment Reliability Supervisor
T. Hough, Maintenance Rule Coordinator
J. Kelsay, Emergency Planning Specialist
G. Kline, Engineering Director
D. Madsen, Licensing Specialist
M. McCormack, Electrical Systems/I&C System Engineering Supervisor
E. McCutchen, Regulatory Affairs Senior Licensing Engineer
M. Metzger, System Engineer
S. Minahan, Vice President - Nuclear & Chief Nuclear Officer
B. Murphy, Emergency Planning Manager
R. Noon, Root Cause Team Leader, Corrective Actions
D. Oshlo, Radiation Protection Manager
S. Rezab, Emergency Planning Specialist
T. Rients, Emergency Planning Specialist
A. Sarver, Balance of Plant Engineering Supervisor
T. Shudak, Fire Protection Program Engineer
T. Stevens, Design Engineering Manager
K. Thomas, Mechanical Programs Supervisor
J. Waid, Training Manager
D. Willis, Operations Manager
AttachmentA-2LIST
: [[OF]] [[]]
: [[ITEMS]] [[]]
: [[OPENED]] [[,]]
: [[CLOSED]] [[,]]
: [[AND]] [[]]
: [[DISCUS]] [[SEDOpened and Closed05000298/2007-001NCVFailure to Survey Radioactive Effluents05000298/2007-002NCVFailure to Promptly Identify and Correct FlowErosion in Service Water Piping05000298/2007-003FINFailure to Follow Requirements of Industrial SafetyProcedures05000298/2007-004NCVInadequate Procedural Guidance to Implement theEmergency PlanClosed05000298/2007-004LERManual Reactor Trip due to Hydraulic Control UnitValve Bonnet Leak into Reactor BuildingLIST]]
: [[OF]] [[]]
: [[DOCUME]] [[NTS]]
: [[REVIEW]] [[]]
: [[EDS]] [[ection 1R04 Equipment Alignments (71111.04) Procedures:NumberDescription      RevisionProcedure 5.8.8Alternate Boron Injection 7with]]
: [[RCI]] [[]]
CSystem Operating Procedure 2.2.67Reactor Core Isolation Cooling System57
System Operating Procedure 2.2.67AReactor Core Isolation Cooling System 19Component ChecklistSystem Operating Procedure 2.2.67BReactor Core Isolation Cooling System1Instrument Valve ChecklistCNS System Health ReportReactor Core Isolation Cooling              June 2007System  June 2007System Operating Procedure 2.2.47A
: [[HV]] [[]]
AC Reactor Building Component 14Checklist
AttachmentA-3System Operating Procedure 2.2.47HVAC Reactor Building41System Operating Procedure 2.2.47BHVAC Reactor Building Instrument4 Valve ChecklistFSAR/USARUSAR, Volume
: [[II]] [[, Section]]
: [[IV]] [[- 7; Reactor Core Isolation Cooling SystemUSAR, Volume IV, Section X-10, Heating, Ventilation and Air Conditioning Systems]]
: [[CNS]] [[System Heath Report; Heating and Ventilation reactor Building; June 2007Drawings and Diagrams]]
BR 2043; Reactor Core Isolation Cooling and Reactor Feed System; Revision N49BR 2020; Reactor Building Heating and Ventilation; Revision N56Corrective Action DocumentsCR-CNS-2007-06443Section 1R19 Postmaintenance Testing (71111.19)Procedures:NumberDescription    RevisionMaintenance Procedure 7.0.8.1System Leakage Testing21Chemistry Procedure 8.4.1.1Post-Accident Sampling System16
Chemistry Procedure
: [[8.PAA.]] [[4Semi-Annual]]
: [[QC]] [[and training for6Post-Accident Sampling SystemSurveillance Procedure]]
: [[RHR]] [[Power Operated Valve Operability Test206.1]]
: [[RHR.]] [[201(IST) (DIV I)Surveillance Procedure Position Indicator Inservice training (IST)136.MISC.401Maintenance Procedure 7.2.30Service Water Zurn Strainer Maintenance9]]
: [[WORK]] [[]]
ORDERS:445795244995974535990
449959544995984501093
4499596445795345836074585698
AttachmentA-4CONDITION
: [[REPORT]] [[S:]]
: [[CR]] [[-CNS-2007-5915SP 6.1]]
: [[DG.]] [[401 completed 8/30/2007]]
: [[CR]] [[-CNS-2007-5916SP 6.1 DG.301 completed 8/31/2007]]
: [[CR]] [[-]]
: [[CNS]] [[-2007-5923]]
: [[CR]] [[-]]
: [[CNS]] [[-2007-5929Section 1R22 Surveillance Testing (71111.22)Procedures:NumberDescriptionRevisionSurveillance Procedure]]
: [[6.SLC.]] [[601]]
SLC Tank Sampling7
Chemistry Procedure 8.7.1.4Boron Potentiometric Analysis 11(High Range)Surveillance Procedure
: [[6.DG.]] [[601]]
DG Fuel Oil Availability14NEDC 97-012Emergency Diesel Generator Fuel 2Oil On-Site Storage Technical
Specification RequirementsSurveillance Procedure 6.1RHR.201RHR Power Operated Valve 20Operability test (IST) (DIV 1)Surveillance Procedure
: [[6.MISC.]] [[401Position Indicator Inservice 13Testing (]]
: [[IST]] [[)Work Orders:4555054, 4535900Section]]
: [[1EP]] [[2 Alert Notification System Testing (711114.02)Emergency Plan Implementing Procedures (]]
EPIP)5.7.21, "Maintaining Emergency Preparedness -Emergency Exercise, Drills, Tests, andEvaluations," Revision 35
5.7.21.1, "NOAA/EAS Radio Malfunction," Revision 9
5.7.27, "Alert and Notification System," Revision 17Administrative Procedure O-EP-02, "Configuration Control of the Automated NotificationSystem (ANS)," Revision 4
AttachmentA-5Alert and Notification System Design Report, Revision 12, May 2004Section
: [[1EP]] [[3 (Emergency Response Organization Augmentation Testing (711114.03)Results of bi-monthly off-hours]]
: [[ERO]] [[call-in drills from 3rd quarter 2005 through 2nd quarter2007, and call-out drill conducted on August 22,]]
: [[2006.E]] [[mergency Plan Implementing Procedures (]]
EPIP)5.7, "Communications," Revision 85.7.2, "Emergency Director Emergency Plan Implementing Procedure," Revision 25
5.7.25, "Recovery Operations," Revision 16Preventive Measure Test Procedure, "Windows
: [[XP]] [[Communicator/ Version 9.3 SystemUpgrade," December 27, 2006Section 1]]
EP5 Correction of Emergency Preparedness Weaknesses and Deficiencies(71114.05)Snapshot Assessment/Benchmark on the Entergy Emergency Preparedness DepartmentDuties and Responsibilities, November 21, 2006.Emergency Planning Department On-going Quarterly Assessment Reports, third quarter 2005through first quarter 2007Quality Assurance Audit Report 06-03, "Emergency Planning," March 13-20, 2006
Quality Assurance Audit Report 07-03, "Emergency Planning," March 12-29, 2007
Apparent Cause Evaluation
: [[CR]] [[-]]
CNS-2006-10569
Root Cause Report, "NOUE Declared in Response to Unverified Fire Alarm," August 24, 2006
Operating Experience Report 23107, "March 1, 2006, Susquehanna Alert, Halon in Vital Area"
Operating Procedure 5.4, "Fire," Revisions 13, 14
Administrative Procedure
: [[O.]] [[39, "Fire Watches," Revision 34Section 2]]
OS1: Access Controls to Radiologically Significant Areas (71121.01) Corrective Action Documents2007-04340, 2007-4933, 2007-05172, 2007-05201, 2007-05297
AttachmentA-6Audits and Self-AssessmentsQAD 20070051Quality Assurance Surveillance Report, "Control of Radiological Work"QAD 20070053Quality Assurance Surveillance Report, "Source Term Reduction andControl" Radiological Department On-Going Assessment Report 1Q2007Radiation Work Permits (or Radiation exposure permit)Procedures9.RADOP.3Area Posting and Access Control, Revision 25
Survey RecordsCNS RP-121Reactor Building - 881' Quads - 6/16/07, 3/06/07, 12/27/06, 9/23/06
MiscellaneousCNS
: [[RP]] [[-11High Radiation Area Gate Key Inventory - 6/29/07, 3/29/07]]
: [[CNS]] [[]]
: [[RP]] [[-39Alarming Dosimeter Set Point FormSection 4]]
OA1 Performance Indicator Verification (71151)Semi-monthly siren test results from July 2006 through June 2007Current training records for 10 designated ERO members
List of qualified ERO members and positions assigned
Critique Reports for Drills and Exercises:Team Evaluated Exercises, July 19 and December 20, 2006Team Evaluated Exercises, March 18, May 16, and July 19, 2007
Operations Crew Simulator Drills, January through June 2007Critique Reports for Declared Events:Notice of Unusual Event, July 25, 2006 and Event Report 42728Notice of Unusual Event, November 11, 2006 and Event Report 42985Emergency Plan Implementing Procedures (EPIP)5.7.1, "Emergency Classification," Revision 355.7.6, "Notification," Revision 43
AttachmentA-75.7.20, "Protective Action Recommendations," Revision 18Emergency Planning Department Guides#2, Attachment G-1, "Emergency Planning Performance Indicator Guide," Revision 12H1, "CNS Drill and Exercise Manual"Section 4OA2 Problem Identification and Resolution (71152)Cooper Nuclear Station Emergency Plan, Revisions 30, 52Cooper Nuclear Station Emergency Action Levels, Revisions 21, 35
Condition Reports:
: [[CR]] [[-]]
CNS-
2006-2416, 2437, 2439, 4508, 5167, 5302, 5303, 5685, 5686, 5722, 5934, 7168, 7222, 7523,10569. 2007- 0071, 0993, 1041, 1886, 2142, 2150, 2237, 2352, 2353, 3562, 4398
AttachmentA-8LIST
: [[OF]] [[]]
: [[ACRONY]] [[MSALARAas low as reasonably achievableCAPcorrective action program]]
: [[CF]] [[]]
RCode of Federal Regulations
DGdiesel generator
DGdiesel generator
: [[EAL]] [[emergency action level]]
EALemergency action level
: [[EP]] [[]]
EPIPemergency plan implementing procedure
IPemergency plan implementing procedure
EROemergency response organization
: [[ERO]] [[emergency response organization]]
FEMAFederal Emergency Management Agency
: [[FEM]] [[]]
AFederal Emergency Management Agency
FINfinding
FINfinding
: [[HWP]] [[hazardous work permit]]
HWPhazardous work permit
: [[ID]] [[]]
IDLHimmediately dangerous to life or health
LHimmediately dangerous to life or health
ISTinservice test
ISTinservice test
LERlicensee event report
LERlicensee event report
: [[NCV]] [[non-cited violation]]
NCVnon-cited violation
: [[NE]] [[]]
NEINuclear Energy Institute
: [[IN]] [[uclear Energy Institute]]
NIOSHNational Institute of Occupational Safety and Health
: [[NIOS]] [[]]
OSHAOccupational Safety and Health Administration
: [[HN]] [[ational Institute of Occupational Safety and Health]]
PPEpersonnel protective equipment
: [[OSH]] [[]]
RCICreactor core isolation cooling
AOccupational Safety and Health Administration
: [[PPE]] [[personnel protective equipment]]
: [[RC]] [[]]
ICreactor core isolation cooling
RHRresidual heat removal
RHRresidual heat removal
: [[SSC]] [[structure, system, and component]]
SSCstructure, system, and component
: [[ST]] [[]]
STELshort term exposure limit
ELshort term exposure limit
TStechnical specification
: [[TS]] [[technical specification]]
UFSARupdated final safety analysis report
: [[UFS]] [[]]
ARupdated final safety analysis report
: [[WO]] [[work order]]
: [[WO]] [[work order]]
}}
}}

Revision as of 01:33, 22 October 2018

IR 05000298-07-004; 06/24/2007 - 09/22/07; Cooper Nuclear Station: Radioactive Gaseous and Liquid Effluent Treatment and Monitoring Systems, Identification and Resolution of Problems, Event Followup
ML072990072
Person / Time
Site: Cooper Entergy icon.png
Issue date: 10/25/2007
From: Hay M C
NRC/RGN-IV/DRP/RPB-C
To: Minahan S B
Nebraska Public Power District (NPPD)
References
IR-07-004
Download: ML072990072 (39)


Text

October 25, 2007

Stewart B. Minahan, Vice President-Nuclear and CNO Nebraska Public Power District P.O. Box 98 Brownville, NE 68321

SUBJECT: COOPER NUCLEAR STATION - NRC INTEGRATED INSPECTION REPORT 05000298/2007004

Dear Mr. Minahan:

On September 22, 2007, the U.S. Nuclear Regulatory Commission (NRC) completed aninspection at your Cooper Nuclear Station. The enclosed integrated inspection report documents the inspection findings which were discussed on October 4, 2007, with Mr. M. Colomb, General Manager of Plant Operations, and other members of your staff.This inspection examined activities conducted under your license as they relate to safety andcompliance with the Commission's rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.Based on the results of this inspection four findings were evaluated under the risk significancedetermination process as having very low safety significance (Green). Three of these findings were determined to be violations of NRC requirements. However, because these violations were of very low safety significance and the issues were entered into your corrective action program, the NRC is treating these findings as noncited violations, consistent with Section VI.A.1 of the NRC's Enforcement Policy. These noncited violations are described in the subject inspection report. If you contest the violations or significance of the violations, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with copies to the Regional Administrator, U.S. Nuclear Regulatory Commission, Region IV, 611 Ryan Plaza Drive, Suite 400, Arlington, Texas 76011-4005; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the Cooper Nuclear Station facility.In accordance with 10 CFR 2.390 of the NRC's Rules of Practice, a copy of this letter, itsenclosure, and your response will be made available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Nebraska Public Power District-2-Should you have any questions concerning this inspection, we will be pleased to discuss themwith you.

Sincerely,/RA/Michael C. Hay, ChiefProject Branch C Division of Reactor ProjectsDocket: 50-298License: DPR-46

Enclosure:

NRC Inspection Report 05000298/2007004

w/Attachment:

Supplemental Information cc w/

Enclosure:

Gene Mace Nuclear Asset Manager Nebraska Public Power District P.O. Box 98 Brownville, NE 68321John C. McClure, Vice President and General Counsel Nebraska Public Power District P.O. Box 499 Columbus, NE 68602-0499David Van Der Kamp Licensing Manager Nebraska Public Power District P.O. Box 98 Brownville, NE 68321Michael J. Linder, DirectorNebraska Department of Environmental Quality P.O. Box 98922 Lincoln, NE 68509-8922 Nebraska Public Power District-3-ChairmanNemaha County Board of Commissioners Nemaha County Courthouse 1824 N Street Auburn, NE 68305Julia Schmitt, ManagerRadiation Control Program Nebraska Health & Human Services Dept. of Regulation & Licensing Division of Public Health Assurance 301 Centennial Mall, South P.O. Box 95007 Lincoln, NE 68509-5007H. Floyd GilzowDeputy Director for Policy Missouri Department of Natural Resources P. O. Box 176 Jefferson City, MO 65102-0176Director, Missouri State Emergency Management Agency P.O. Box 116 Jefferson City, MO 65102-0116Chief, Radiation and Asbestos Control Section Kansas Department of Health and Environment Bureau of Air and Radiation 1000 SW Jackson, Suite 310 Topeka, KS 66612-1366Melanie Rasmussen, State Liaison Officer/Radiation Control Program Director Bureau of Radiological Health Iowa Department of Public Health Lucas State Office Building, 5th Floor 321 East 12th Street Des Moines, IA 50319John F. McCann, Director, LicensingEntergy Nuclear Northeast Entergy Nuclear Operations, Inc.

440 Hamilton Avenue White Plains, NY 10601-1813 Nebraska Public Power District-4-Keith G. Henke, PlannerDivision of Community and Public Health Office of Emergency Coordination 930 Wildwood, P.O. Box 570 Jefferson City, MO 65102Paul V. Fleming, Director of Nuclear Safety Assurance Nebraska Public Power District P.O. Box 98 Brownville, NE 68321 Nebraska Public Power District-5-Electronic distribution by RIV:Regional Administrator (EEC)DRP Director (ATH)DRS Director (DDC)DRS Deputy Director (RJC1)Senior Resident Inspector (NHT)Branch Chief, DRP/C (MCH2)Senior Project Engineer, DRP/C (WCW)Team Leader, DRP/TSS (CJP)RITS Coordinator (MSH3)Only inspection reports to the following:DRS STA (DAP)D. Pelton, OEDO RIV Coordinator (DLP)ROPreports CNS Site Secretary (SEF1)SUNSI Review Completed: WCW ADAMS:

X Yes __ No Initials: WCW X Publicly Available __ Non-Publicly Available ___ Sensitive X Non-SensitiveR:\_REACTORS\_CNS\2007\CN2007-04RP-NHT.wpdSRI:DRP/CC:SPE:DRP/CC:DRS/EB1C:DRS/PSBC:DRS/OBNHTaylorWCWalkerWBJonesMPShannonATGody/E-WCWalker for/ /RA/ /RA/ /RA/ /RA/10/25/0710/25/0710/22/0710/22/0710/22/07C:DRS/EB2C:DRP/CLJSmithMCHay/RA DLProulx for/ /RA/10/22/0710/25/07OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax Enclosure-1-U.S. NUCLEAR REGULATORY COMMISSIONREGION IV Docket:50-298 License:DPR-46 Report:05000298/2007004 Licensee:Nebraska Public Power District Facility:Cooper Nuclear Station Location:P.O. Box 98 Brownville, Nebraska Dates:June 24 through September 22, 2007 Inspectors:N. Taylor, Senior Resident InspectorM. Chambers, Resident Inspector R. Lantz, Senior Emergency Preparedness Inspector L. Ricketson, P.E., Senior Health Physicist R. Cohen, Resident InspectorApproved By:M. Hay, Branch C, Division of Reactor Projects Enclosure-2-

SUMMARY OF FINDINGS

IR 05000298/2007004; 06/24/2007 - 09/22/07; Cooper Nuclear Station: Radioactive Gaseousand Liquid Effluent Treatment And Monitoring Systems, Identification and Resolution of

Problems, Event Followup.The report covered a 3-month period of inspection by resident inspectors and region-basedinspectors. Three Green noncited violations and one Green finding were identified. The significance of most findings is indicated by their color (Green, White, Yellow, or Red) using Inspection Manual Chapter 0609, "Significance Determination Process." Findings for which the significance determination process does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 3, dated July 2000.A.

NRC-Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

Green.

The inspectors identified a Green finding regarding the licensee's failure tofollow the requirements of industrial safety procedures. Specifically, licensee personnel violated the requirements of Administrative Procedure 0.36, "Industrial Safety Procedure," and Administrative Procedure 0.36.6, "Monitoring for Industrial Gases," during a chemical injection treatment in the service water system. Specifically, the licensee failed to properly post the hazardous work permit, the individuals performing the work did not review the permit, and licensee personnel did not immediately evacuate the work area as required following a toxic gas release. This issue was entered into the licensee's corrective action program as Condition Report CR-CNS-2007-06421.The finding is more than minor because if left uncorrected it could become a moresignificant safety concern in that failure to follow industrial safety procedures during chlorine dioxide injections could put personnel at significant risk of injury and could have resulted in a larger toxic gas release in the intake structure, inhibiting the operators'

ability to access safety related equipment to mitigate the consequences of an accident.

Using Inspection Manual Chapter 0609, Appendix A, "Determining the Significance of Reactor Inspection Findings for At-Power Situations," the finding was determined to be of very low safety significance because it did not result in a loss of safety function for any mitigating system. The cause of this finding is related to the human performance cross cutting component of work practices in that licensee personnel did not follow the requirements of industrial safety procedures as required (H.4(b)). (Section 4OA3)

Green.

The inspectors identified a noncited violation of 10 CFR 50, Appendix B,Criterion XVI, "Corrective Action," regarding the licensee's failure to promptly identify and correct a condition adverse to quality. Specifically, a degraded condition that was discovered in the service water supply piping to Diesel Generator 2 on August 16, 2007, was not evaluated for its effect on the operability of Diesel Generator 2 until prompted Enclosure-4-by inspectors on August 17, 2007. As a result, additional unavailability time wasnecessary to repair the degraded condition. This issue was entered into the licensee's corrective action program as Condition Report CR-CNS-2007-05590.The finding is more than minor because if left uncorrected, the flow erosion of the DieselGenerator 2 service water supply piping could have become a more significant safety concern. Using Inspection Manual Chapter 0609, Appendix A, "Determining the Significance of Reactor Inspection Findings for At-Power Situations," the finding was determined to be of very low safety significance because it did not represent an actual loss of safety function of the diesel generator for greater than its technical specification allowed outage time. The cause of this finding is related to the problem identification and resolution cross cutting component of corrective action program in that the licensee did not correct the degraded condition of the Diesel Generator 2 service water piping in a timely manner (P.1(a)). (Section 4OA2)

Cornerstone: Emergency Preparedness

Green.

The inspectors identified a noncited violation of 10 CFR 50.47 (b)(4) regardingthe licensee's failure to establish adequate procedural guidance to implement the emergency plan. Specifically, Emergency Plan Implementing Procedure 5.7.1,

"Emergency Classification", Revision 35, contained inadequate procedural guidance in that it did not identify any specific entry criteria for Emergency Action Level 5.1.2. This issue was entered into the licensee's corrective action program as Condition Report CR-CNS-2007-05135.The finding is more than minor because it is associated with the EmergencyPreparedness cornerstone attribute of procedural quality and affects the associated cornerstone objective to ensure that the licensee is capable of implementing adequate measures to protect the health and safety of the public in the event of a radiological emergency. Using Inspection Manual Chapter 0609, Appendix B, "Emergency Preparedness Significance Determination Process," the finding was determined to be of very low safety significance since the EAL classification process that was in place prior to August 30, 2007 could have resulted in a failure to declare a Notification of Unusual Event when it should have been declared. The cause of this finding is related to the human performance cross cutting component of resources in that complete and accurate procedures were not adequately maintained to support the emergency plan (H.2(c)). (Section 4OA3)

Cornerstone: Public Radiation Safety

Green.

The inspector identified a noncited violation of 10 CFR 20.1302(a) because thelicensee's surveys of effluents containing radioactive particulates originating in the multi-purpose facility were not adequate to ensure compliance with the dose limits for individual members of the public required by 10 CFR 20.1301. The surveys were not adequate because the configuration of the radioactive effluent monitoring system in the multi-purpose facility was changed in 2007, and the sampling lines in the new configuration were not analyzed for line loss. The licensee documented the situation in the corrective action program and declared the multi-purpose facility effluent monitoring system inoperable. Further corrective action is being evaluated.

Enclosure-5-The finding is greater than minor because it is associated with the Public RadiationSafety Cornerstone attribute of equipment and instrumentation and affects the cornerstone objective in that the failure to perform adequate surveys of radioactive effluents could result in increased public dose. When processed through the Public Radiation Safety Significance Determination Process, the finding was determined to be of very low safety significance because it: (1) was not a radioactive material control finding, (2) was an effluent release program finding, (3) impaired the licensee's ability to assess dose, (4) it did not result in a failure to assess dose, (5) did not result in public doses that exceeded the values of 10 CFR Part 50, Appendix I, or 10 CFR 20.1301(d).

In addition, this finding had cross-cutting aspects in the area of human performance and the component of resources because the licensee did not ensure complete, accurate, and up-to-date design documentation requests and specifications were supplied to outsourced engineering providers. (H.2.(c)) (Section 2PS1)

Enclosure-6-

REPORT DETAILS

Summary of Plant StatusThe plant began the inspection period at 100 percent power. On August 11, 2007, reactorpower was reduced to approximately 70 percent for a planned rod pattern exchange and surveillance testing. During the power ascension, one of four circulating water discharge valves stuck shut, and as a result the licensee held power at approximately 93 percent. On August 13, 2007, the licensee returned to full power and remained there for the rest of the inspection period.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and EmergencyPreparedness1R04 Equipment Alignment (71111.04Q)

.1 Partial System Walkdown

a. Inspection Scope

The inspectors:

(1) walked down portions of the two risk important systems listed belowand reviewed plant procedures and documents to verify that critical portions of the selected systems were correctly aligned; and
(2) compared deficiencies identified during the walkdown to the licensee's UFSAR and the licensee's CAP to ensure problems were being identified and corrected. *August 7, 2007, Division II Residual Heat Removal (RHR) during plannedmaintenance on Div 1RHR*September 18, 2007, Reactor Core Isolation Cooling (RCIC) during HighPressure Coolant Injection MaintenanceThe inspectors completed two samples.

b. Findings

No findings of significance were identified.

.2 Complete System Walkdown

a. Inspection Scope

The inspectors:

(1) reviewed plant procedures, drawings, the UFSAR, TSs, and vendormanuals to determine the correct alignment of the Reactor Building Ventilation System;
(2) reviewed outstanding design issues, operator workarounds, and UFSAR documents

-7-to determine if open issues affected the functionality of the Reactor Building VentilationSystem; and

(3) verified that the licensee was identifying and resolving equipment alignment problems.*September 19, 2007, Reactor Building Ventilation System The inspectors completed one sample.

b. Findings

No findings of significance were identified.

1R05 Fire Protection

Fire Protection Tours (71111.05Q)

a. Inspection Scope

The inspectors walked down the six plant areas listed below to assess the materialcondition of active and passive fire protection features and their operational lineup and readiness. The inspectors:

(1) verified that transient combustibles and hot work activities were controlled in accordance with plant procedures;
(2) observed the condition of fire detection devices to verify they remained functional;
(3) observed fire suppression systems to verify they remained functional and that access to manual actuators was unobstructed;
(4) verified that fire extinguishers and hose stations were provided at their designated locations and that they were in a satisfactory condition; (5)verified that passive fire protection features (electrical raceway barriers, fire doors, fire dampers, steel fire proofing, penetration seals, and oil collection systems) were in a satisfactory material condition;
(6) verified that adequate compensatory measures were established for degraded or inoperable fire protection features and that the compensatory measures were commensurate with the significance of the deficiency; and
(7) reviewed the UFSAR to determine if the licensee identified and corrected fire protection problems. *July 11, 2007, Fire Zone 20A, Service Water Pump Room*July 25, 2007, Fire Zone 9B, Cable Expansion Room
  • July 25, 2007, Fire Zone 1G, Hydraulic Drive Pump Area
  • August 10, 2007, Fire Zone 20A, Service Water Pump Room During B Strainer Cleaning*September 20, 2007, Fire Zone 1A, RCIC and Core Spray Pump RoomDocuments reviewed by the inspectors included:

Administrative Procedure 0.23, CNS Fire Protection Plan, Revision 49 The inspectors completed six samples.

-8-

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification (71111.11Q)

a. Inspection Scope

The inspectors observed testing and training of senior reactor operators and reactoroperators to identify deficiencies and discrepancies in the training, to assess operator performance, and to assess the evaluator's critique. The inspectors' observations were performed on August 10, 2007 by monitoring control rod manipulation during a scheduled downpower and an effectiveness review of requalification training.The inspectors completed one sample.

b. Findings

No findings of significance were identified.

1R12 Maintenance Rule (711111.12Q)

a. Inspection Scope

The inspectors reviewed the maintenance effectiveness performance issues listed belowto:

(1) verify the appropriate handling of structure, system, and component (SSC)performance or condition problems;
(2) verify the appropriate handling of degraded SSC functional performance;
(3) evaluate the role of work practices and common cause problems; and
(4) evaluate the handling of SSC issues reviewed under the requirements of the maintenance rule, 10 CFR Part 50, Appendix B, and the TSs.*September 4, 2007, CRD-V-101(25-27) leakage on May 19, 2007*September 4, 2007, Failure of Division 1 Service Water Strainer on August 1, 2007Documents reviewed by the inspectors included:
  • Functional Failure Evaluations for functions CRD-F02A and CRD-V-F03a*Functional Failure Evaluations for functions SW-F01A and SW01C
  • CR-CNS-2007-05210The inspectors completed two samples.

b. Findings

No findings of significance were identified.

-9-1R13Maintenance Risk Assessments and Emergent Work Evaluation (71111.13)

a. Inspection Scope

The inspectors reviewed the three maintenance activities listed below to verify: (1)performance of risk assessments when required by 10 CFR 50.65 (a)(4) and licensee procedures prior to changes in plant configuration for maintenance activities and plant operations;

(2) the accuracy, adequacy, and completeness of the information considered in the risk assessment;
(3) that the licensee recognized, and/or entered as applicable, the appropriate licensee-established risk category according to the risk assessment results and licensee procedures; and
(4) the licensee identified and corrected problems related to maintenance risk assessments.*June 28, 2007, Reactor Vessel Level Control System Troubleshooting*August 7, 2007, Work on RHR-MOV-13A
  • Work Order (WO) 4572910*Administrative Procedure 0.49, "Schedule Risk Assessment," Rev. 19
  • Administrative Procedure O-PROTECT-EQP, "Protected Equipment Program,"Rev. 5*CR-CNS-2007-05331The inspectors completed three samples.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations (71111.15)

a. Inspection Scope

The inspectors:

(1) reviewed operator shift logs, emergent work documentation,deferred modifications, and standing orders to determine if an operability evaluation was warranted for degraded components;
(2) referred to the UFSAR and other design basis documents to review the technical adequacy of licensee operability evaluations; (3)evaluated compensatory measures associated with operability evaluations; (4)determined degraded component impact on any TSs;
(5) used the Significance Determination Process to evaluate the risk significance of degraded or inoperable equipment; and
(6) verified that the licensee has identified and implemented appropriate corrective actions associated with degraded components.

-10-The following equipment performance issues were reviewed: *July 10, 2007, Diesel Generator (DG) 1 Operability with High Service WaterSediment Levels*August 15, 2007, DG 2 Service Water Piping Leak

  • August 30, 2007, DG Lubricating Oil and Jacket Water Heat Exchanger TubePlugs Over-torqued*September 7, 2007, DG 1 Operability Common Cause Review
  • September 11, 2007, DG 1 Operability Following Day Tank Level Control SystemFailureDocuments reviewed by the inspectors included:
  • CR-CNS-2007-05571*CR-CNS-2007-05875
  • CR-CNS-2007-04688
  • CR-CNS-2007-06143The inspectors completed five samples.

b. Findings

No findings of significance were identified.

1R19 Postmaintenance Testing (71111.19)

a. Inspection Scope

The inspectors selected four post-maintenance tests associated with the maintenanceactivities listed below for risk significant systems or components. For each item, the inspectors:

(1) reviewed the applicable licensing basis and/or design basis documentsto determine the safety functions;
(2) evaluated the safety functions that may have been affected by the maintenance activity; and
(3) reviewed the test procedure to ensure it adequately tested the safety function that may have been affected. The inspectors either witnessed or reviewed test data to verify that acceptance criteria were met, plant impacts were evaluated, test equipment was calibrated, procedures were followed, jumpers were properly controlled, the test data results were complete and accurate, the test equipment was removed, the system was properly re-aligned, and deficiencies during testing were documented. The inspectors also reviewed the UFSAR to determine if the licensee identified and corrected problems related to postmaintenance testing. *August 3, 2007, Post-Accident Sampling System following relief valvereplacements and valve rebuilds*August 7, 2007, RHR-MOV-13A test following motor pinion inspection/repair
  • August 10, 2007, Service Water B zurn strainer following inspection
  • August 16, 2007, DG 2 Service Water piping repairThe inspectors completed four samples.

-11-

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors reviewed the UFSAR, procedure requirements, and TSs to ensure thatthe three surveillance activities listed below demonstrated that the SSCs tested were capable of performing their intended safety functions. The inspectors either witnessed or reviewed test data to verify that the following significant surveillance test attributes were adequate:

(1) preconditioning;
(2) evaluation of testing impact on the plant; (3)acceptance criteria;
(4) test equipment;
(5) procedures;
(6) jumper/lifted lead controls;
(7) test data;
(8) testing frequency and method demonstrated TS operability;
(9) test equipment removal;
(10) restoration of plant systems;
(11) fulfillment of American Society Mechanical Engineers Code requirements;
(12) engineering evaluations, root causes, and bases for returning tested SSCs not meeting the test acceptance criteria were correct;
(13) reference setting data; and
(14) annunciators and alarms setpoints.

The inspectors also verified that the licensee identified and implemented any needed corrective actions associated with the surveillance testing.*August 1, 2007, DG Fuel Oil Availability*August 6, 2007, Standby Liquid Control Tank Sample

  • August 7, 2007, RHR-MO-13A following motor pinion inspectionThe inspectors completed three samples.

b. Findings

No findings of significance were identified.1EP2Alert Notification System Testing (71114.02)

a. Inspection Scope

The inspector discussed with licensee staff the status of offsite siren and tone alert radiosystems to determine the adequacy of licensee methods for testing the alert and notification system in accordance with 10 CFR 50, Appendix E, "Emergency Planning and Preparedness." The inspector observed a monthly siren test on July 24, 2007, performed from the Emergency Operation Facility. The licensee's alert and notification system testing program was compared with criteria in NUREG-0654, "Criteria for Preparation and Evaluation of Radiological Emergency Response Plans and Preparedness in Support of Nuclear Power Plants," Revision 1, Federal Emergency Management Agency (FEMA) Report REP-10, "Guide for the Evaluation of Alert and Notification Systems for Nuclear Power Plants," and the licensee's current FEMA-approved alert and notification system design report. The inspector also reviewed the references listed in the Attachment to this report.

-12-The inspector completed one sample during the inspection.

b. Findings

No findings of significance were identified.1EP3Emergency Response Organization Augmentation Testing (71114.03)

a. Inspection Scope

The inspector discussed with licensee staff the status of primary and backup systemsfor augmenting the on-shift emergency response staff to determine the adequacy of licensee methods for staffing emergency response facilities. The inspector reviewed the references listed in the Attachment to this report related to the emergency response organization (ERO) augmentation system to evaluate the licensee's ability to staff the emergency response facilities in accordance with the licensee emergency plan and the requirements of 10 CFR 50 Appendix E.The inspector completed one sample during the inspection.

b. Findings

No findings of significance were identified.1EP5Correction of Emergency Preparedness Weaknesses and Deficiencies (71114.05)

a. Inspection Scope

The inspector reviewed the licensee's corrective action program (CAP) requirements inAdministrative Procedure 0.5.CR, "Condition Report Initiation, Review, and Classification," Revision 7. The inspector reviewed summaries of approximately 200 condition reports assigned to the emergency planning department during calendar years 2006 and 2007, and selected 26 for detailed review against the program requirements.

The inspector evaluated the response to the corrective action requests to determine the licensee's ability to identify, evaluate, and correct problems in accordance with the licensee program requirements and 10 CFR 50.47(b)(14) and 10 CFR 50 Appendix E.

The inspector also reviewed other documents listed in the attachment to this report.The inspector completed one sample during the inspection.

b. Findings

No findings of significance were identified.2.RADIATION SAFETYCornerstone: Occupational Radiation Safety [OS]

-13-2OS1Access Control To Radiologically Significant Areas (71121.01)

a. Inspection Scope

This area was inspected to assess the licensee's performance in implementing physicaland administrative controls for airborne radioactivity areas, radiation areas, high radiation areas, and worker adherence to these controls. The inspector used the requirements in 10 CFR Part 20, the technical specifications, and the licensee's procedures required by technical specifications as criteria for determining compliance.

During the inspection, the inspector interviewed the radiation protection manager, radiation protection supervisors, and radiation workers. The inspector performed independent radiation dose rate measurements and reviewed the following items:*Radiation work permits, procedures, engineering controls, and air samplerlocations*Conformity of electronic personal dosimeter alarm set points with surveyindications and plant policy; workers' knowledge of required actions when their electronic personnel dosimeter noticeably malfunctions or alarms *Barrier integrity and performance of engineering controls in airborne radioactivityareas*Physical and programmatic controls for highly activated or contaminatedmaterials (non-fuel) stored within spent fuel and other storage pools. *Self-assessments, audits, licensee event reports, and special reports related tothe access control program since the last inspection*Corrective action documents related to access controls

  • Licensee actions in cases of repetitive deficiencies or significant individualdeficiencies *Radiation work permit briefings and worker instructions
  • Adequacy of radiological controls, such as required surveys, radiation protectionjob coverage, and contamination control during job performance *Dosimetry placement in high radiation work areas with significant dose rategradients*Changes in licensee procedural controls of high dose rate - high radiation areasand very high radiation areas*Controls for special areas that have the potential to become very high radiationareas during certain plant operations

-14-*Posting and locking of entrances to all accessible high dose rate - high radiationareas and very high radiation areas*Radiation worker and radiation protection technician performance with respect toradiation protection work requirements *Either because the conditions did not exist or an event had not occurred, noopportunities were available to review the following item:*Adequacy of the licensee's internal dose assessment for any actual internalexposure greater than 50 millirem committed effective dose equivalent The inspector completed 18 of the required 21 samples.

b. Findings

No findings of significance were identified.2OS2ALARA Planning and Controls (71121.02)

a. Inspection Scope

The inspector assessed licensee performance with respect to maintaining individual andcollective radiation exposures as low as is reasonably achievable (ALARA). The inspector used the requirements in 10 CFR Part 20 and the licensee's procedures required by technical specifications as criteria for determining compliance. The inspector interviewed licensee personnel and reviewed:*Current 3-year rolling average collective exposure

  • Assumptions and basis for the current annual collective exposure estimate, themethodology for estimating work activity exposures, the intended dose outcome, and the accuracy of dose rate and man-hour estimates*Declared pregnant workers during the current assessment period, monitoringcontrols, and the exposure results*Self-assessments, audits, and special reports related to the ALARA programsince the last inspectionDocuments reviewed by inspector included:

Condition Reports:2007-05267, 2007-05268Procedures*9.ALARA.5ALARA Planning and Controls, Revision 17*9.ALARA.9Dose Determination to the Embryo/Fetus, Revision 0

-15-The inspector completed 4 of the required 15 samples.

b. Findings

No findings of significance were identified.2PS1Radioactive Gaseous and Liquid Effluent Treatment And Monitoring Systems(71122.01)

a. Inspection Scope

This area was inspected to ensure that the gaseous and liquid effluent processingsystems are maintained so that radiological releases are properly mitigated, monitored, and evaluated with respect to public exposure. The inspector used the requirements in 10 CFR Part 20, 10 CFR Part 50 Appendices A and I, the Offsite Dose Calculation Manual, and the licensee's procedures required by technical specifications as criteria fordetermining compliance. The inspector interviewed licensee personnel and reviewed: *Effluent monitoring system modifications Documents reviewed by inspector included:

  • NEDC 92-207- Kaman Radiation Monitor Sample Line Plate Out Calculation
  • Change Evaluation Document 6015500 - Multi-Purpose Facility Kaman EffluentMonitor Replacement*Drawing Number: SKE-6015500-01, Revision BThe inspector completed 1 of the required 11 samples.

b. Findings

Introduction.

The inspector identified a noncited violation of 10 CFR 20.1302(a)because the licensee's surveys of effluents containing radioactive particulates were not adequate to ensure compliance with the dose limits for individual members of the public in 10 CFR 20.1301. The violation had very low safety significance.Description. The licensee replaced the instruments used to detect radioactiveparticulates and iodine in the multi-purpose facility ventilation exhaust with sampling filters. The design modification on the effluent monitoring system became operational February 13, 2007. During a walkdown of the sampling system, the inspector noted the licensee modified the sampling line configuration through the introduction of a tee in the line to allow switching of the air flow to either the A or B sampler. Following interviews and a review of design change documents, the inspector determined the licensee had not reviewed the design changes using the same methodology, from ANSI 13.1 - 1969, "American National Standard Guide to Sampling Airborne Radioactive Materials in Nuclear Facilities," it committed to using when the effluent monitoring instrumentation was originally installed. ANSI 13.1 - 1969 states, "Elbows in sampling lines should be avoided, if at all possible."

-16-In response, the licensee documented the problem in the CAP, declared themulti-purpose facility effluent monitoring system inoperable, and performed an apparent cause evaluation. The apparent cause evaluation identified two contributing factors.

The design change was "outsourced" and the work request or task agreement contained no instructions the design needed to conform to the ANSI 13.1 - 1969 methodology. Also, the design preparer (vendor) and reviewer (in-house) had the mindset the design was downgraded with less stringent design requirements.The licensee walked down the effluent sampling lines to determine the extent ofcondition and found the remaining sampling lines met the ANSI 13.1 - 1969 guidelines, with the exception of those to the alternate samplers in the turbine, radwaste, and reactor buildings. The alternate samplers also used tee connectors. (Condition Report 2007-05726, Corrective Action 2 will address the alternate sampler configuration.)Analysis. The licensee made changes to a previously analyzed effluent samplingsystem without updating its analysis to determine the effect on iodine plateout and particle deposition of placing a 90 degree bend in effluent sampling lines. Because the licensee had not followed the ANSI guidance for system analysis nor tested the final configuration to determine the effect on particulate sampling, it could not confirm its sampling results were representative of multi-purpose facility effluent releases. Without representative samples, the licensee could not adequately perform an evaluation or survey. The failure to survey effluents is a performance deficiency. The finding is associated with one of the Public Radiation Safety cornerstone attributes (plant equipment and instrumentation) and affects the associated cornerstone objective, in that the failure to survey effluents for radioactivity could lead to increased public dose. The finding involved an occurrence in the licensee's radiological effluent monitoring program that is contrary to NRC regulations. When processed through the Public Radiation Safety Significance Determination Process, the finding was determined to be of very low safety significance because it:

(1) was not a radioactive material control problem, (2)was an effluent release program problem,
(3) impaired the licensee's ability to assess dose,
(4) did not result in a total failure to assess dose because the licensee had other means of assessing the effects of particulate and iodine on public dose, and
(5) did not result in public doses that exceeded the values of 10 CFR Part 50, Appendix I, or 10 CFR 20.1301(d). In addition, this finding had cross-cutting aspects in the area of human performance and the component of resources because the licensee did not ensure complete, accurate, and up-to-date design documentation requests and specifications were supplied to outsourced engineering providers. (H.2.(c))Enforcement. Part 20.1302(a) of Title 10 of the Code of Federal Regulations requiresthe licensee make or cause to be made, as appropriate, surveys of radiation levels in unrestricted and controlled areas and radioactive materials in effluents released to unrestricted and controlled areas to demonstrate compliance with the dose limits for individual members of the public in 10 CFR 20.1301. The licensee violated 10 CFR 20.1302(a) when they made surveys of radioactive materials in effluents released to unrestricted areas using samples which could not be verified as representative of the effluent stream. This violation was entered into the licensee's CAP by Condition Reports CR-2007-05726 and CR-2007-05733. Because this violation was determined to be of

-17-very low safety significance and was entered into the licensee's CAP, it is being treatedas a noncited violation, consistent with Section VI.A of the NRC Enforcement Policy:

NCV 05000298/2007004-01, "Failure to Survey Radioactive Effluents".4.OTHER ACTIVITIES

4OA1 Performance Indicator Verification

a. Inspection Scope

Cornerstone: Emergency PreparednessThe inspector reviewed licensee evaluations for the three emergency preparednesscornerstone performance indicators of Drill and Exercise Performance, ERO Participation, and Alert and Notification System Reliability, for the period July 1, 2006 through June 30, 2007. The definitions and guidance of the Nuclear Energy Institute (NEI) 99-02, "Regulatory Assessment Indicator Guideline," Revisions 3 and 4, and the licensee Performance Indicator Procedure 0-PI-1, "Performance Indicator Program,"

Revision 20, were used to verify the accuracy of the licensee's evaluations for each performance indicator reported during the assessment period. The inspector reviewed a sample of drill and exercise scenarios and licensed operatorsimulator training sessions, notification forms, and attendance and critique records associated with training sessions, drills, and exercises conducted during the verification period. The inspector reviewed selected emergency responder qualification, training, and drill participation records. The inspector reviewed alert and notification system testing procedures, maintenance records, and a 100 percent sample of siren test records. The inspector also reviewed other documents listed in the Attachment to this report. The inspector completed three samples during the inspection.

Cornerstone : Occupational Radiation SafetyOccupational Exposure Control Effectiveness The inspector reviewed licensee documents from April 1 through June 30, 2007. Thereview included corrective action documentation that identified occurrences in locked high radiation areas (as defined in the licensee's technical specifications), very high radiation areas (as defined in 10 CFR 20.1003), and unplanned personnel exposures (as defined in Nuclear Energy Institute (NEI) 99-02, "Regulatory Assessment Indicator Guideline," Revision 4). Additional records reviewed included ALARA records and whole body counts of selected individual exposures. The inspector interviewed licensee personnel that were accountable for collecting and evaluating the performance indicator data. In addition, the inspector toured plant areas to verify that high radiation, locked high radiation, and very high radiation areas were properly controlled. Performance indicator definitions and guidance contained in NEI 99-02, Revision 4, were used to verify the basis in reporting for each data element.

-18-The inspector completed the required sample

(1) in this cornerstone.

Cornerstone:

Public Radiation SafetyRadiological Effluent Technical Specification/Offsite Dose Calculation Manual Radiological Effluent Occurrences The inspector reviewed licensee documents from April 1 through June 30, 2007.Licensee records reviewed included corrective action documentation that identified occurrences for liquid or gaseous effluent releases that exceeded performance indicator thresholds and those reported to the NRC. The inspector interviewed licensee personnel that were accountable for collecting and evaluating the performance indicator data. Performance indicator definitions and guidance contained in NEI 99-02, Revision 4, were used to verify the basis in reporting for each data element.The inspector completed the required sample

(1) in this cornerstone.

b. Findings

No findings of significance were identified.4OA2Problem Identification and Resolution (71152)

.1 Emergency Preparedness Problem Identification and Resolution

a. Inspection Scope

The inspector selected 26 condition reports for detailed review. The condition reportswere reviewed to ensure that the full extent of the issues were identified, an appropriate evaluation was performed, and appropriate corrective actions were specified and prioritized. The inspector evaluated the condition reports and corrective actions against the requirements of Administrative Procedure 0.5.CR, "Condition Report Initiation, Review, and Classification," Revision 7.

b. Findings and Observations

No findings of significance were identified.

.2 Access Control and ALARA Planning and Controls

a. Inspection Scope

The inspector evaluated the effectiveness of the licensee's problem identification andresolution process with respect to the following inspection areas:*Access Control to Radiologically Significant Areas (Section 2OS1)*ALARA Planning and Controls (Section 2OS2)

-19-

b. Findings and Observations

No findings of significance were identified.

.3 Selected Issue Follow-up Inspection

a. Inspection Scope

In addition to the routine review, the inspectors selected the issues listed below for amore in-depth review. The inspectors considered the following during the review of the licensee's actions:

(1) complete and accurate identification of the problem in a timely manner;
(2) evaluation and disposition of operability/reportability issues; (3)consideration of extent of condition, generic implications, common cause, and previous occurrences;
(4) classification and prioritization of the resolution of the problem; (5)identification of root and contributing causes of the problem;
(6) identification of corrective actions; and
(7) completion of corrective actions in a timely manner. *July 27, 2007, RHR 13D declutch mechanism failure*July 31, 2007, Simulator modeling error
  • August 17, 2007, Flow Erosion in DG2 Service Water PipingDocuments reviewed by inspectors included:
  • CR-CNS-2007-05070*CR-CNS-2007-03569
  • CR-CNS-2007-05624The inspectors completed three samples.

b. Findings

Introduction.

The inspectors identified a Green NCV regarding the licensee's failure topromptly identify and correct a condition adverse to quality. Specifically, a degraded condition was discovered in the service water supply piping to DG2 but was not evaluated for its effect on the operability of DG2 until prompted by inspectors on August 17, 2007. As a result, additional unavailability time was necessary to repair the degraded condition.Description. On August 16, 2007, during a planned surveillance test of DG2, licenseepersonnel discovered a through-wall leak in the service water supply piping to DG2. As a result of the through-wall leak in the piping, the licensee declared both loops of service water inoperable due to cross-connected nature of the system. Shortly thereafter, the licensee closed a normally open cross connect valve, splitting the two service water loops and restoring the operability of service water loop A. This left DG2 and service water loop B inoperable and the licensee began planning a repair. In preparation for the repair, licensee personnel conducted an ultrasonic survey of thearea surrounding the leak for the purpose of determining the most appropriate repair method. As a precaution, the surrounding piping was also surveyed for indications of

-20-pipe wall thinning. This survey revealed an additional area of pipe that appeared to beless than the minimum wall thickness of 0.111 inches. The estimated thickness at this location was 0.1 inches.This additional indication was discussed during the planning process for the through-wallleak. As documented in CR-CNS-2007-05624, the licensee considered the options available to address the degraded condition of the service water piping in DG2. While there was recognition that an additional degraded condition existed beyond the through-wall leak, the licensee elected not to attempt a repair of this area because the necessary replacement parts had not yet been received. The decision was made to repair only the through-wall leak. This repair was planned and completed by Work Order 4583607 during the night shift on August 16. DG2 was loaded for a post-maintenance test at 0247 on August 17, 2007.Upon reporting to the site on the morning of August 17, the inspectors noted thediscussion in the outage control center logs about the second indication of wall thinning below minimum wall thickness. The inspectors challenged the licensee regarding this additional indication and learned that the condition had not been entered into the CAP, nor had it been evaluated for its impact on the operability of DG2. In response to the inspector's concerns, the licensee conducted an additional ultrasonic survey of the DG2 piping and discovered that the area in question was worn to between 0.06 and 0.08 inch remaining wall thickness, approximately half of minimum wall thickness. Based upon this information, the licensee elected to tag out DG2 again and perform a more extensive internal repair of the eroded service water piping. This repair was completed and service water loop B was declared operable at 2021 on August 17, 2007. DG2 was subsequently declared operable at 2104 on August 17, 2007.The through-wall leak was assumed to be a contemporary manifestation of thepreviously-observed flow erosion in this section of the service water piping caused by high flow velocity. As a result of the historical erosion at this location, the licensee's preventative maintenance program requires an ultrasonic inspection of the piping each operating cycle. The inspectors reviewed the results of the most recent inspection of this location, performed September 17, 2006. The inspectors noted that the ultrasonic test did not reveal the fact that either of the areas that required repair in August 2007 were showing signs of wall thinning in September 2006.The inspectors noted that in response to this event, the licensee has initiated correctiveactions to improve the preventative maintenance tasks for inspecting this section of piping and evaluate the service water system for other areas vulnerable to flow induced erosion. In addition, new materials are being considered for improved resistance to flow induced erosion in this section of piping.Analysis. The performance deficiency associated with this finding involved thelicensee's failure to promptly identify and correct a condition adverse to quality. The finding is more than minor because if left uncorrected, the flow erosion of the DG2 service water supply piping could have become a more significant safety concern.

Using Inspection Manual Chapter 0609, Appendix A, "Determining the Significance of Reactor Inspection Findings for At-Power Situations," the finding was determined to be

-21-of very low safety significance because it did not represent an actual loss of safetyfunction of the diesel generator for greater than its technical specification allowed outage time. The cause of this finding is related to the problem identification and resolution cross-cutting component of CAP in that the licensee did not identify and correct the degraded condition of the DG2 service water piping in a timely manner (P.1(a)).Enforcement. 10 CFR 50, Appendix B, Criterion XVI, "Corrective Action," requires, inpart, that measures be established to assure that conditions adverse to quality are promptly identified and corrected. Contrary to this, a degraded condition was discovered in the service water supply piping to DG2 on August 16, 2007, but was not corrected until the licensee was prompted by inspectors on August 17, 2007. As a result, additional unavailability time was necessary to repair the degraded condition.

Because the finding is of very low safety significance and has been entered into the licensee's CAP as Condition Report CR-CNS-2007-05590, this violation is being treated as an NCV consistent with Section VI.A of the Enforcement Policy: NCV 05000298/2007004-002, "Failure to Promptly Identify and Correct Flow Erosion in Service Water Piping".4OA3Event Follow-up (71153)

.1 Failure to Follow Requirements of Industrial Safety Procedures

a. Inspection Scope

The inspectors reviewed the licensee's response to a toxic gas release on site on July 27, 2007. The inspectors reviewed the licensee's control of the evolution through work control documents, established procedures and operating logs. The followup inspection also reviewed the cause of the release and the licensee's corrective actions.Documents reviewed by inspectors included:

  • Administrative Procedure 0.36, "Industrial Safety Procedure," Revision 28*Administrative Procedure 0.36.6, "Monitoring for Industrial Gases," Revision 4
  • WO 4559451
  • CR-CNS-2007-05169
  • CR-CNS-2007-06241

b. Findings

Introduction.

The inspectors identified a Green finding regarding the licensee's failureto follow the requirements of industrial safety procedures. Specifically, licensee personnel violated the requirements of Administrative Procedure 0.36, "Industrial Safety Procedure," and Administrative Procedure 0.36.6, "Monitoring for Industrial Gases,"

during a chemical injection treatment in the service water system.Description. On July 27, 2007, the licensee commenced a chemical treatmentprocedure per WO 4559451 in an effort to mitigate previously identified macro-fouling in

-22-the safety-related service water system. The chemical treatment was being performedby a contractor overseen by station personnel, using a temporary system designed to inject high concentrations of chlorine and chlorine dioxide into the service water system.

The temporary system included several gaseous concentration monitors designed to warn personnel if potentially dangerous chemical leaks were present.In preparation for this procedure, the supervising engineer prepared a hazardous workpermit (HWP) as required by Administrative Procedure 0.36, "Industrial Safety Procedure," Revision 28. Step 3.33.1 states that:"In order to establish these controls, the HWP should be used to controlconditions, specify necessary engineering controls, compensatory measures, or Personal Protective Equipm ent (PPE) to be used, ...."In addition, step 3.33.4 states that:"The Hazardous Work Permit Supplementary Time Report Form (Attachment 2)serves as the record (i.e. sign in log) for personnel entering an HWP controlled area, provides special instructions, and provides a record..."Contrary to these requirements, the HWP generated for WO 4559451 did not list allchemicals to which maintenance personnel would be exposed. Specifically, the processgenerated chlorine gas, which was not listed in the HWP, and as such personnel were not briefed on the hazards, exposure limits or appropriate PPE. Additionally, the HWP was not maintained at the job site and was not reviewed and signed by the personnel doing the work in the field. As a result, those personnel did not get the full benefit of the safety information and instructions written on the form.In addition, station personnel failed to follow the requirements of Procedure 0.36.6,"Monitoring for Industrial Gases," Revision 4, following receipt of a valid toxic gas alarm in the intake structure on July 29, 2007. During the chemical treatment process, a leak developed in the temporary chlorination piping, resulting in an airborne release of chlorine and chlorine dioxide gases. The locally installed mulit-gas alarm went off and indicated a general area chlorine dioxide concentration at the short term exposure limit of 0.3 ppm for chlorine dioxide. Procedure 0.36.6 provides a warning in section 4 prohibiting entry into a work space if a hazardous atmosphere is indicated. In addition, step 4.5 requires that "if at any time while working within the confined space the monitor alarms, evacuate the work space immediately." Contrary to these requirements, the maintenance personnel did not exit the space in light of the chlorine dioxide gas alarm.

Instead, they used the alarming instrument to walk down the piping and look for the leak without donning any PPE, putting themselves at risk of significant personal injury. In addition, had the maintenance personnel become incapacitated, station operators could have been exposed to a toxic gas environment during the conduct or their normal duties or during event response. The failure to follow the station's industrial safety procedures could have affected the availability of systems necessary to mitigate the consequences of an accident, specifically the safety-related portions of the service water system located within the intake structure.

-23-In response to these concerns from the inspectors, the licensee initiated CR-CNS-2007-05169, which resulted in creating a more thorough HWP to be used in future chemical injection efforts. In addition, the licensee initiated CR-CNS-2007-06241 to address the improper response of maintenance personnel to the receipt of toxic gas alarms in the intake structure.Analysis. The performance deficiency associated with this finding involved thelicensee's failure follow the requirements of Procedure 0.36, "Industrial Safety Procedure," and Procedure 0.36.6, "Monitoring for Industrial Gases." The finding is more than minor because if left uncorrected, it could become a more significant safety concern if not corrected in that failure to follow industrial safety procedures during chlorine dioxide injections could put personnel at significant risk of injury and could have resulted in a larger toxic gas release in the intake structure, inhibiting operators' ability to access safety related equipment to mitigate the consequences of an accident. Using Inspection Manual Chapter 0609, Appendix A, "Determining the Significance of Reactor Inspection Findings for At-Power Situations," the finding was determined to be of very low safety significance because it did not result in a loss of safety function for any mitigating system.The cause of this finding is related to the human performance cross cutting componentof work practices in that licensee personnel did not follow the requirements of industrial safety procedures as required (H.4(b)).Enforcement. No violation of NRC requirements was identified. This finding is identifiedas FIN 05000298/2007004-003, "Failure to Follow Requirements of Industrial Safety Procedures."

.2 Inadequate Procedural Guidance to Implement Emergency Plan

a. Inspection Scope

The inspectors reviewed the licensee's response to a toxic gas release on site on July 27, 2007. The inspectors reviewed the licensee's control of the evolution through work control documents, established procedures and operating logs. In addition, the inspectors reviewed the event for compliance with the station Emergency Plan. The followup inspection also reviewed the cause of the release and the licensee's corrective actions.Documents reviewed by inspectors included:

  • Emergency Plan Implementing Procedure 5.7.1.7, "Classification," Revision 35*CR-CNS-2007-05135

b. Findings

Introduction.

The inspectors identified a Green NCV regarding the licensee's failure toestablish adequate procedural guidance to implement the emergency plan.

-24-Description. On July 27, 2007, the licensee commenced a chemical treatmentprocedure in an effort to mitigate previously identified macro-fouling in the safety-related service water system. The chemical treatment was being performed by a contractor using a temporary system designed to inject high concentrations of chlorine and chlorine dioxide into the service water system. The temporary system included several gaseous concentration monitors designed to warn personnel if potentially dangerous chemical leaks were present.During the treatment on July 29, 2007, a local gaseous concentration alarm went off,warning personnel that chlorine and chlorine dioxide gas were leaking into the intake structure. The maximum general area concentrations recorded by the instrument were 0.3 ppm chlorine dioxide and 0.3 ppm chlorine. The temporary system was immediately secured and the source of the leak was found. This information was reported to control room operators, who determined that the gaseous leak did not meet the entry criteria for any emergency action levels (EALs) listed in Emergency Plan Implementing Procedure 5.7.1, "Emergency Classification." (EPIP 5.7.1). EPIP 5.7.1, Revision 35, Attachment 2 provided the following guidance for classifying toxic gas release events:

EALClassificationText 5.1.2NOUEReport or detection of toxic or flammable gas that couldenter the Protected Area in amounts that will affect the health of plant personnel or can affect normal plant operations.5.2.2ALERTReport or detection of toxic or flammable gas within a VitalArea in concentrations that will be life threatening to plant personnel or will affect the safe operation of the plant.The inspectors noted that additional information was provided in EPIP 5.7.1 to clarify theentry criterion for EAL 5.2.2. Specifically, the EPIP page for EAL 5.2.2 contained the following additional guidance: "IDLH atmospheres (for Toxic gases)...in Vital Areas should be considered as meeting this condition." The inspectors noted that no such clarifying guidance was provided for EAL 5.1.2.The inspectors reviewed the operating logs and discussed the event with operations andemergency planning staff to gain an understanding of the information available to the operators and the rationale used in implementing the emergency plan. The inspectors noted that the operators justified not declaring an event by comparing the immediately dangerous to life or health (IDLH) limits for the toxic gases to the highest concentrations seen in the field. The inspectors determined that this was an appropriate threshold for EAL 5.2.2, but challenged the licensee's treatment of EAL 5.1.2 given the lower threshold described in the EAL 5.1.2 text.Concentrations limits below IDLH have been defined by the Occupational Safety andHealth Administration (OSHA) and National Institute for Occupational Safety and Health(NIOSH). OSHA and NIOSH define the short-term exposure limits (STEL) of 0.3 ppm for chlorine dioxide and 0.5 ppm for chlorine (for comparison, the IDLH concentrations for these gases are 5 ppm for chlorine dioxide and for 10 ppm chlorine). The NIOSH

-25-standard states that exposures above the STEL concentrations should not exceedfifteen minutes based on the risk of severe respiratory and eye irritation.The inspectors determined that this represented a technical inadequacy in EPIP 5.7.1,in that no specific entry criteria were defined in the EPIP to allow the Emergency Director to determine whether or not toxic gas concentrations were present in "amounts that will affect the health of plant personnel" as described in the EAL 5.1.2 text. This procedural weakness was demonstrated on July 29, 2007, when the concentration of chlorine and chlorine dioxide gas were compared only to IDLH limits during the event classification process. In response to this issue, on August 30, 2007, the licensee revised EPIP 5.7.1 to provide clarification on the entry criteria for EALs 5.1.2 and 5.2.2.

In addition, the licensee created a required reading task for all control room operators to ensure they understood the technical issue and the new guidance.Based on a review of information collected by the licensee and interviews with personnelwho were present at the time of the chemical leak, the inspectors concluded that on July 29, 2007, the gas monitor being used to detect toxic gas conditions alarmed and indicated that the concentration of chlorine dioxide gas in the intake structure had reached the STEL limit of 0.3 ppm. The leak was immediately secured, after which the monitor was used to locate the specific source of the leak. Chlorine dioxide levels as high as 1.0 ppm were identified during the search for the leak. The licensee has determined that using the new guidance in EPIP 5.7.1, this event would not have resulted in an entry into EAL 5.1.2 due to the fact that the gas monitor was taking a suction approximately eight inches above the floor level and was not representative of the breathing zone to which personnel were exposed.The inspectors reviewed the revision history for EPIP 5.7.1, and noted that periodicreview conducted as required by Administrative Procedure 0.4A,"Procedure Change Process Supplement", Revision 14, did not identify this error. Specifically, the person completing the required periodic review on November 14, 2005, errantly determined that a review of the entire EPIP was not required, and as such missed an opportunity to identify this procedural shortcoming.Analysis. The performance deficiency associated with this finding involved thelicensee's failure to maintain adequate procedural guidance to implement the emergency plan. The finding is more than minor because it is associated with the Emergency Preparedness cornerstone attribute of procedural quality and affects the associated cornerstone objective to ensure that the licensee is capable of implementing adequate measures to protect the health and safety of the public in the event of a radiological emergency. Using Inspection Manual Chapter 0609, Appendix B, "Emergency Preparedness Significance Determination Process," the finding was determined to be of very low safety significance since the EAL classification process that was in place prior to August 30, 2007, could have resulted in a failure to declare a Notification of Unusual Event when it should have been declared. The cause of this finding is related to the human performance cross cutting componentof resources in that complete and accurate procedures were not adequately maintained to support the emergency plan (H.2(c)).

-26-Enforcement. 10 CFR 50.47 (b)(4) requires, in part, that a standard emergencyclassification and action level scheme is in use by the nuclear facility licensee. Contrary to this, Emergency Plan Implementing Procedure 5.7.1, "Emergency Classification",

Revision 35, contained inadequate procedural guidance in that it did not identify any specific entry criteria for Emergency Action Level 5.1.2. As a result, the conditions requiring entry into Emergency Action Level 5.1.2 could have existed without the proper event classification being made. Because the finding is of very low safety significance and has been entered into the licensee's CAP as Condition Report CR-CNS-2007-05135, this violation is being treated as an NCV consistent with Section VI.A of the Enforcement Policy: NCV 05000298/2007004-004, "Inadequate Procedural Guidance to Implement the Emergency Plan"..3(Closed) LER 50-298/2007-004: Manual Reactor Trip due to Hydraulic Control UnitValve Bonnet Leak into Reactor BuildingOn May 19, 2007, during disassembly of a directional control valve on a control rod drivesystem hydraulic control unit, a water leak developed. Control room operators inserted a manual reactor scram when the leak changed from water to steam and was unable to be isolated. The cause of the leak was a combination of a degraded condition in an upstream isolation valve and a failure by the licensee to implement vendor guidance in isolating the hydraulic control unit for maintenance. This event and the ensuing violation of NRC requirements are discussed in detail in NRC Integrated Inspection Report 05000298/2007003. This LER is closed.4OA6Meetings, Including ExitOn July 26, 2007, a regional inspector conducted an exit meeting to present the resultsof the emergency preparedness program inspection to Mr. M. Colomb, General Manager, Plant Operations. The inspector confirmed that proprietary information was not provided or examined during the inspection.On August 24, 2007, a regional inspector presented the occupational radiation safetyinspection results to Mr. M. Colomb, General Manager, Plant Operations and other members of his staff who acknowledged the findings. The inspector confirmed that proprietary information was not provided or examined during the inspection.On October 4, 2007, the resident inspectors conducted an exit meeting to present theresults of the emergency preparedness program inspection to Mr. M. Colomb, General Manager, Plant Operations and other members of his staff who acknowledged the findings. The inspector confirmed that proprietary information was not provided or examined during the inspection.ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

A. Alexander, Emergency Planning Specialist
T. Bahensky, System Engineer
J. Bebb, Security Manager
J. Bednar, Staff Health Physicist, Radiation Protection
R. Beilke, Chemistry Manager
V. Bhardwaj, Engineering Support Manager
D. Buman, Systems Engineering Manager
T. Carson, Maintenance Manager
J. Christensen, Support General Manager
M. Colomb, Plant Operations General Manager
R. Dyer, Heat Exchanger Program Engineer
J. Dykstra, Electrical Engineering Program Supervisor
T. Erickson, System Engineering Supervisor
R. Estrada, Corrective Action Program Manager
K. Fike, Plant Chemist, Chemistry
J. Flaherty, Senior Licensing Engineer
P. Fleming, Nuclear Safety Assurance Director
K. Garner, Radiological Operations Supervisor, Radiation Protection
T. Haynes, Emergency Planning Specialist
T. Hottovy, Equipment Reliability Supervisor
T. Hough, Maintenance Rule Coordinator
J. Kelsay, Emergency Planning Specialist
G. Kline, Engineering Director
D. Madsen, Licensing Specialist
M. McCormack, Electrical Systems/I&C System Engineering Supervisor
E. McCutchen, Regulatory Affairs Senior Licensing Engineer
M. Metzger, System Engineer
S. Minahan, Vice President - Nuclear & Chief Nuclear Officer
B. Murphy, Emergency Planning Manager
R. Noon, Root Cause Team Leader, Corrective Actions
D. Oshlo, Radiation Protection Manager
S. Rezab, Emergency Planning Specialist
T. Rients, Emergency Planning Specialist
A. Sarver, Balance of Plant Engineering Supervisor
T. Shudak, Fire Protection Program Engineer
T. Stevens, Design Engineering Manager
K. Thomas, Mechanical Programs Supervisor
J. Waid, Training Manager
D. Willis, Operations Manager

AttachmentA-2

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and

Closed

05000298/2007-001NCVFailure to Survey Radioactive Effluents05000298/2007-002NCVFailure to Promptly Identify and Correct FlowErosion in Service Water Piping05000298/2007-003FINFailure to Follow Requirements of Industrial SafetyProcedures05000298/2007-004NCVInadequate Procedural Guidance to Implement theEmergency Plan

Closed

05000298/2007-001NCVFailure to Survey Radioactive Effluents05000298/2007-002NCVFailure to Promptly Identify and Correct FlowErosion in Service Water Piping05000298/2007-003FINFailure to Follow Requirements of Industrial SafetyProcedures05000298/2007-004NCVInadequate Procedural Guidance to Implement theEmergency Plan

LIST OF DOCUMENTS REVIEWED

Section 1R04 Equipment Alignments (71111.04) Procedures

NumberDescription
RevisionProcedure 5.8.8Alternate Boron Injection 7with RCICSystem Operating Procedure 2.2.67Reactor Core Isolation Cooling System57
System Operating Procedure 2.2.67AReactor Core Isolation Cooling System 19Component ChecklistSystem Operating Procedure 2.2.67BReactor Core Isolation Cooling System1Instrument Valve ChecklistCNS System Health ReportReactor Core Isolation Cooling
June 2007System
June 2007System Operating Procedure 2.2.47A
HVAC Reactor Building Component 14Checklist AttachmentA-3System Operating Procedure 2.2.47HVAC Reactor Building41System Operating Procedure 2.2.47BHVAC Reactor Building Instrument4 Valve ChecklistFSAR/USARUSAR, Volume II,Section IV - 7; Reactor Core Isolation Cooling SystemUSAR, Volume IV, Section X-10, Heating, Ventilation and Air Conditioning Systems
CNS System Heath Report; Heating and Ventilation reactor Building; June 2007Drawings and DiagramsBR 2043; Reactor Core Isolation Cooling and Reactor Feed System; Revision N49BR 2020; Reactor Building Heating and Ventilation; Revision N56Corrective Action DocumentsCR-CNS-2007-06443Section 1R19 Postmaintenance Testing (71111.19)Procedures:NumberDescription
RevisionMaintenance Procedure 7.0.8.1System Leakage Testing21Chemistry Procedure 8.4.1.1Post-Accident Sampling System16
Chemistry Procedure 8.PAA.4Semi-Annual QC and training for6Post-Accident Sampling SystemSurveillance Procedure RHR Power Operated Valve Operability Test206.1RHR.201(IST) (DIV I)Surveillance Procedure Position Indicator Inservice training (IST)136.MISC.401Maintenance Procedure 7.2.30Service Water Zurn Strainer Maintenance9
WORK ORDERS
445795244995974535990
449959544995984501093
449959644579534583607
4585698
AttachmentA-4CONDITION REPORTS
CR-CNS-2007-5915SP 6.1
DG.401 completed 8/30/2007CR-CNS-2007-5916SP 6.1
DG.301 completed 8/31/2007
CR-CNS-2007-5923
CR-CNS-2007-5929Section 1R22 Surveillance Testi ng (71111.22)Procedures
NumberDescriptionRevisionSurveillance Procedure 6.SLC.601SLC Tank Sampling7
Chemistry Procedure 8.7.1.4Boron Potentiometric Analysis 11(High Range)Surveillance Procedure 6.DG.601DG Fuel Oil Availability14NEDC 97-012Emergency Diesel Generator Fuel 2Oil On-Site Storage Technical Specification RequirementsSurveillance Procedure 6.1RHR.201RHR Power Operated Valve 20Operability test (IST) (DIV 1)Surveillance Procedure 6.MISC.401Position Indicator Inservice 13Testing (IST)Work Orders:4555054, 4535900Section 1EP2 Alert Notification System Testing (711114.02)Emergency Plan Implementing Procedures (EPIP)5.7.21, "Maintaining Emergency Preparedness -Emergency Exercise, Drills, Tests, andEvaluations," Revision 35
5.7.21.1, "NOAA/EAS Radio Malfunction," Revision 9
5.7.27, "Alert and Notification System," Revision 17Administrative Procedure O-EP-02, "Configuration Control of the Automated NotificationSystem (ANS)," Revision 4
AttachmentA-5Alert and Notification System Design Report, Revision 12, May 2004Section 1EP3 (Emergency Response Organization Augmentation Testing (711114.03)Results of bi-monthly off-hours ERO call-in drills from 3rd quarter 2005 through 2nd quarter2007, and call-out drill conducted on August 22, 2006.Emergency Plan Implementing Procedures (EPIP)5.7, "Communications," Revision 85.7.2, "Emergency Director Emergency Plan Implementing Procedure," Revision 25
5.7.25, "Recovery Operations," Revision 16Preventive Measure Test Procedure, "Windows XP Communicator/ Version 9.3 SystemUpgrade," December 27, 2006Section 1EP5 Correction of Emergency Preparedness Weaknesses and Deficiencies(71114.05)Snapshot Assessment/Benchmark on the Entergy Emergency Preparedness DepartmentDuties and Responsibilities, November 21, 2006.Emergency Planning Department On-going Quarterly Assessment Reports, third quarter 2005through first quarter 2007Quality Assurance Audit Report 06-03, "Emergency Planning," March 13-20, 2006
Quality Assurance Audit Report 07-03, "Emergency Planning," March 12-29, 2007
Apparent Cause Evaluation CR-CNS-2006-10569
Root Cause Report, "NOUE Declared in Response to Unverified Fire Alarm," August 24, 2006

Operating Experience

Report 23107, "March 1, 2006, Susquehanna Alert, Halon in Vital Area" Operating Procedure 5.4, "Fire," Revisions 13, 14
Administrative Procedure O.39, "Fire Watches," Revision 34

Section 2OS1: Access Controls to Radiologically Significant Areas (71121.01) Corrective Action Documents2007-04340, 2007-4933, 2007-05172, 2007-05201, 2007-05297

AttachmentA-6Audits and Self-AssessmentsQAD 20070051Quality Assurance Surveillance Report, "Control of Radiological Work"QAD 20070053Quality Assurance Surveillance Report, "Source Term Reduction andControl" Radiological Department On-Going Assessment Report 1Q2007Radiation Work Permits (or Radiation exposure permit)Procedures9.RADOP.3Area Posting and Access Control, Revision 25
Survey RecordsCNS
RP-121Reactor Building - 881' Quads - 6/16/07, 3/06/07, 12/27/06, 9/23/06
MiscellaneousCNS
RP-11High Radiation Area Gate Key Inventory - 6/29/07, 3/29/07CNS
RP-39Alarming Dosimeter Set Point FormSection 4OA1 Performance Indicator Verification (71151)Semi-monthly siren test results from July 2006 through June 2007Current training records for 10 designated ERO members List of qualified ERO members and positions assigned Critique Reports for Drills and Exercises:Team Evaluated Exercises, July 19 and December 20, 2006Team Evaluated Exercises, March 18, May 16, and July 19, 2007
Operations Crew Simulator Drills, January through June 2007Critique Reports for Declared Events:Notice of Unusual Event, July 25, 2006 and Event Report 42728Notice of Unusual Event, November 11, 2006 and Event Report 42985Emergency Plan Implementing Procedures (EPIP)5.7.1, "Emergency Classification," Revision 355.7.6, "Notification," Revision 43
AttachmentA-75.7.20, "Protective Action Recommendations," Revision 18Emergency Planning Department Guides#2, Attachment G-1, "Emergency Planning Performance Indicator Guide," Revision 12H1, "CNS Drill and Exercise Manual"Section 4OA2 Problem Identification and Resolution (71152)Cooper Nuclear Station Emergency Plan, Revisions 30, 52Cooper Nuclear Station Emergency Action Levels, Revisions 21, 35
Condition Reports:
CR-CNS-
2006-2416, 2437, 2439, 4508, 5167, 5302, 5303, 5685, 5686, 5722, 5934, 7168, 7222, 7523,10569.
2007- 0071, 0993, 1041, 1886, 2142, 2150, 2237, 2352, 2353, 3562, 4398
AttachmentA-8

LIST OF ACRONYMS

ALARAas low as reasonably achievableCAPcorrective action program

CFRCode of Federal Regulations

DGdiesel generator

EALemergency action level

EPIPemergency plan implementing procedure

EROemergency response organization

FEMAFederal Emergency Management Agency

FINfinding

HWPhazardous work permit

IDLHimmediately dangerous to life or health

ISTinservice test

LERlicensee event report

NCVnon-cited violation

NEINuclear Energy Institute

NIOSHNational Institute of Occupational Safety and Health

OSHAOccupational Safety and Health Administration

PPEpersonnel protective equipment

RCICreactor core isolation cooling

RHRresidual heat removal

SSCstructure, system, and component

STELshort term exposure limit

TStechnical specification

UFSARupdated final safety analysis report

WO work order