NL-03-1455, June 2003 Monthly Operating Report for Edwin I. Hatch
| ML031960162 | |
| Person / Time | |
|---|---|
| Site: | Hatch |
| Issue date: | 07/10/2003 |
| From: | Sumner H Southern Nuclear Operating Co |
| To: | Document Control Desk, Office of Nuclear Reactor Regulation |
| References | |
| NL-03-1455 | |
| Download: ML031960162 (7) | |
Text
H. L Sumner, Jr.
Vice President Hatch Project Southern Nuclear Operating Company, Inc.
Post Office Box 1295 Birmingham, Alabama 35201 Tel 205.992.7279 4
SOUTHERNA COMPANY Energy to Serve Your World'>
NL-03-1455 July 10, 2003 Docket Nos.:
50-321 50-366 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D. C. 20555-0001 Edwin I. Hatch Nuclear Plant Monthly Operating Reports Ladies and Gentlemen:
Enclosed are the June 2003 Monthly Operating Reports as required by Section 5.6.4 of the Technical Specifications.
If you have any questions, please advise.
H. L. Sumner, Jr.
HLSfIL/daj
Enclosures:
El - HNP Unit 1 Monthly Operating Report E2 - HNP Unit 2 Monthly Operating Report cc:
Southern Nuclear Operating Company Mr. J. D. Woodard, Executive Vice President Mr. G. R. Frederick, General Manager - Plant Hatch Document Services RTYPE: CHA02.004 U. S. Nuclear Regulatory Commission Mr. L. A. Reyes, Regional Administrator Mr. S. D. Bloom, NRR Project Manager - Hatch Mr. D. S. Simpkins, Senior Resident Inspector - Hatch
q Plant Hatch Unit 1 Monthly Operating Report June 2003 Table of Contents Page Operating Data Report El-i Unit Shutdowns and Power Reductions E1-2
OPERATING DATA REPORT Docket No.:
Unit Name:
Date:
Completed By:
Telephone:
50-321 E.. Hatch Unit 1 July 1, 2003 S. B. Rogers (912) 366-2000 x2279 Operating Status
- 1. Reporting Period:
- 2. Design Electrical Rating (Net MWe):
- 3. Maximum Dependable Capacity (Net MWe):
JUNE 2003 870 856 This Month
- 4. Number of Hours Reactor Was Critical:
- 5. Hours Generator On Line:
- 6. Unit Reserve Shutdown Hours:
- 7. Net Electrical Energy Generated:
720.0 720.0 0.0 620,691 Year To Date 4,037.5 4,021.0 0.0 3,399,099 Cumulative 194,455.8 188,493.8 0.0 137,930,347 CHALLENGES TO MAIN STEAM SAFETY I RELIEF VALVES Date Tag No.
Event Description (YYMMDD)
No challenges this month.
E1-1
UNIT SHUTDOWNS Docket No.:
Unit Name:
Date:
Completed By:
Telephone:
50-321 E.. Hatch Unit 1 July 1, 2003 S. B. Rogers (912) 366-2000 x2279 Reporting Period:
JUNE 2003 Type Method of Date F: Forcd Duration Shutling Cause/Corrective Actions No.
MYMMDD)
Scheduld (Hours)
Reason (1)
Down (2)
Comments No unit shutdowns occurred this month.
(1) Reason:
(2) METHOD A-Equipment Failure (Explain) 1-Manual B-Maintenance or Test 2-Manual Trip/Scram C-Refueling 3-Automatic TriplScram D-Regulatory Restriction 4-Continuation E-Operator Training/License Examination 5-Other (Explain)
F-Administrative G-Operational Error (Explain)
H-Other (Explain)
CAUSE/CORRECTIVE ACTIONICOMMENTS:
NARRATIVE REPORT
-~~~~~~~~~~~
Unit I began the month of June operating at rated thermal power. Shift reduced load to approximately 875 GMWe
(-2748 CMWU) on June 13 after the "A" Reactor Feed Pump Minimum Flow Valve failed partially open. The minimum flow line was isolated and the unit was returned to rated thermal power later that day. Shift reduced load to approximately 820 GMWe (-2540 CMWT) on June 14 to perform control rod drive exercises. The unit was returned to rated thermal power on June 15. Shift reduced load to approximately 890 GMWe (-2705 CMWQ) on June 22 to perform main turbine valve testing. The unit was returned to rated thermal power later that day. Shift reduced load to approximately 805 GMWe (-2430 CMWT) on June 23 when power was momentarily lost to the fans on the Helper Cooling Tower, due to a faulted transformer, and main condenser vacuum began to degrade. The fans cycled back on as designed, and the unit was returned to rated thermal power later the same day. Shift maintained unit operation at rated thermal power for the remainder of the month.
E1-2
Plant Hatch Unit 2 Monthly Operating Report June 2003 Table of Contents Page Operating Data Report Unit Shutdowns and Power Reductions E2-1 E2-2
OPERATING DATA REPORT Docket No.:
Unit Name:
Date:
Completed By:
Telephone:
50-366 E.. Hatch Unit 2 July 1, 2003 S. B. Rogers (912) 366-2000 x2279 Oneratinq Status
- 1. Reporting Period:
- 2. Design Electrical Rating (Net MWe):
- 3. Maximum Dependable Capacity (Net MWe):
JUNE 2003 894 870 This Month Year To Date Cumulative
- 4. Number of Hours Reactor Was Critical:
- 5. Hours Generator On Line:
- 6. Unit Reserve Shutdown Hours:
- 7. Net Electrical Energy Generated:
720.0 714.2 0.0 605,525 3,676.7 3,635.6 0.0 3,115,995 170,343.9 165,955.5 0.0 123,733,897 CHALLENGES TO MAIN STEAM SAFETY I RELIEF VALVES Date Tag No.
Event Description (YYMMDD)
No challenges this month.
E2-1
UNIT SHUTDOWNS Docket No.:
Unit Name:
Date:
Completed By:
Telephone:
50-366 E.. Hatch Unit 2 July 1, 2003 S. B. Rogers (912) 366-2000 x2279 Reporting Period:
JUNE 2003 Type Method of Date F: Forced Duration Shutting Cause/Corrective Actions No.
(VYMMDD)
S: Sdwduled (Hours)
Reason (1)
Down (2)
Comments03-003 030621 F
5.8 A
5 The main generator was removed from the grid to repair a leak on a filter in the Stator Cooling Water System.
The leak was repaired and the main generator was re-tied to the grid (1) Reason:
(2) METHOD A-Equipment Failure (Explain) 1-Manual B-Maintenance or Test 2-Manual Trip/Scram C-Refueling
.3-Automatic Trip/Scram D-Regulatory Restriction 4-Continuation E-Operator Training/License Examination 5-Other (Explain)
F-Administrative G-Operational Error (Explain)
H-Other (Explain)
CAUSE/CORRECTIVE ACTIONICOMMENTS:
NARRATIVE REPORT Unit 2 began the month of June operating at rated thermal power. Shift reduced load to approximately 550 GMWe
(-1795 CMWT) on June 13 to perform a control rod sequence exchange, scram time testing, control rod drive exercises, and main turbine valve testing. Inspection and maintenance activities were also performed in the condenser bay while at reduced load. The unit was returned to rated thermal power on June 14. Shift reduced reactor power to approximately 22% of rated thermal on June 21 and removed the main generator from the grid to facilitate the repair of a leak on a filter in the Stator Cooling Water System. Shift re-tied the main generator to the grid on June 21 and returned the unit to rated thermal power on June 22. Shift reduced load to approximately 855 GMWe (-2625 CMWT) on June 23 for a rod pattern adjustment. The unit was returned to rated thermal power later that day. Shift reduced load to approximately 815 GMWe (-2430 CMWT) on June 23 when power was momentarily lost to the fans on the Helper Cooling Tower, due to a faulted transformer, and main condenser vacuum began to degrade. The fans cycled back on as designed, and the unit was returned to rated thermal power later the same day. Shift maintained unit operation at rated thermal power for the remainder of the month.
E2-2