ML20198H209

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SALP Rept 50-213/85-98 for Mar 1985 - Feb 1986.Overall Performance Acceptable
ML20198H209
Person / Time
Site: Haddam Neck File:Connecticut Yankee Atomic Power Co icon.png
Issue date: 02/28/1986
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20198H191 List:
References
50-213-85-98, NUDOCS 8605300157
Download: ML20198H209 (76)


See also: IR 05000213/1985098

Text

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t.NCLOSURE 2

U.S. NUCLEAR REGULATORY COMMISSION

REGION I

SYSTEMATIC ASSESSMENT OF LICENSEE JERFORMANCE

INSPECTION REPORT 50-213/8f.-98

CONNECTICUT YANKEE ATOMIC POWER COMPANY

HADDAM NECK NUCLEAR POWER PLANT

ASSESSMENT PERIOD: MARCH 1, 1985 - FEBRUARY 28, 1986

BOARD MEETING DATE: APRIL 24, 1986

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TABLE OF CONTENTS

Page-

1.

INTRODUCTION..........................................................

1

A.

Purpose and 0verview.............................................

1

B.

SALP Board Members...............................................

1

C.

Background..... ...................................... ..........

2

II.

CRITERIA..............................................................

4

III. SUMMARY OF RESULTS....................................................

6

A.

Facility Performance.........................

...................

6

B.

Overall Facility Eva1aution......................................

6

IV.

PERFORMANCE ANALYSIS..................................................

7

A.

Plant 0perations.................................................

7

B.

Radiological

Controls.........................

.................

11

C.

Mai ntenance and Modi fi cati ons. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

15

D.

Survei11ance....................................................

18

E.

Emergency' Preparedness..........................................

20

F.

Security and Safeguards.........................................

22.

G.

Refueling and Outage Management.................................

24

H.

Assurance of Quality............................................

26

I.

Training and Qualification Effectiveness........................

28

J.

Licensing Activities............................................

30

V.

SUPPORTING DATA AND SUMMARIES........................................

32

A.

Investigation and Allegation Review.............................

32

B.

Escalated Enforcement Action....................................

32

C.

Management Conferences..........................................

32

D.

Licensee Event Reports..........................................

33

E.

Operating Reactors Licensing Actions. . . . . . . . . . . . . . . . . . . . . . . . . . . .

34

-TABLES

Table 1 - Tabular Listing of LERs by Functional Area

Table 2 - LER Synopsis

Table 3 - Inspection Hours Summary

Table 4 - Enforcement Summary

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Table 5 - Enforcement Data

Table 6 - Inspection Activities

. Table 7 - Plant Shutdowns

FIGURE

Figure 1 - Number of Days Shut Down Per Month

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I.

INTRODUCTION

A.

Purpose and Overview

The Systematic Assessment of Licensee Performance (SALP) is an integrated

NRC staff effort to collect information periodically and evaluate licen-

see performance.

SALP supplements the normal regulatory processes that

ensure compliance with NRC regulations.

It is intended to be sufficiently

diagnostic to provide a rational basis for allocation of.NRC resources

and to be meaningful-to licensee efforts to improve safety.

An NRC SALP Board met on April 24, 1986 to perform this SALP in accord-

ance with NRC Manual Chapter 0516, " Systematic Assessment of Licensee

Performance." A summary of the SALP guidance is provided in Section II

of this report.

This report assesses performance at the Haddam Neck Plant during the 12-

month period from March 1, 1985 through February 28, 19_86.

B.

SALP Board Members

Chairman:

W. F. Kane, Deputy Director, Division of Reactor Projects (DRP)

Members:

T. T. Martin, Director, Division of Radiation Safety and Safeguards,

(DRSS)

L. H. Bettenhausen, Chief, Operations Branch, Division of Reactor Safety

(DRS)

R. R. Bellamy, Chief, Emergency Preparedness and Radiological Protection

Branch, DRSS

E. C. Wenzinger, Chief, Projects Branch 3, DRP

E. C. McCabe, Chief, Reactor Projects Section 3B, DRP

P. D. Swetland, Senior Resident Inspector, Haddam Neck

C. I. Grimes, Director, Integrated Safety Assessment Project Directorate,

Office of Nuclear Reactor Regulation (NRR) (by telecon)

F. M. Akstulewicz, Licensing Project Manager, NRR

Other Attendees

M. M. Shanbaky, Chief, Facilities Radiation Protection Section, DRSS

T. F. Dragoun, Radiation Specialist

M._C. Kray, Reactor Engineer

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C.

Background

1.

Licensee Activities

At the beginning of this SALP period on March 1, 1985, the facility had

been operating at or near full power (600 MWe) since November 22, 1984.

Full power operation continued until March 12, 1985.

On March 12, the licensee began reducing load to 50% when a ground in

the "B" condensate pump motor caused a halon system discharge in the

switchgear room.

Later that day, a reactor trip from 50% power occurred

on high reactor coolant system pressure because load was being rapidly

reduced to compensate for a loss of feedwater control caused by a failed

open main feedwater (MFW) pump recirculation control valve.

On March

16, after return to 100% power, the plant was manually tripped due to

a large leak in the MFW piping between the "1B" feedwater heater normal

level control valve and its downstream isolation valve.

Following re-

placement of the ruptured section of MFW piping, 100% power operation

was resumed from March 20 until April 13, when load was reduced to 50%

to repair the "B" condensate pump motor.

Full power operation resumed

the next day.

On May 16, there was a manual reactor and turbine trip

from 100% power because two control rods dropped into the reactor core

during manual control rod movement.

No cause for the rod drops was

identified.

During the post-trip approach to criticality, main turbine

generator excitation problems delayed startup until May 18, when full

power was attained.

On August 18, the plant was shut down to replace

the leaking "A" MFW pump inboard seal.

Full power operation resumed from

August 21 until September 27 when the plant was shut down for Hurricane

Gloria.

No significant site damage was experienced during the hurricane.

The plant was returned to 100% power on September 30.

On November 3, an extended power coastdown to 90% power began.

On Novem-

ber 10, an automatic reactor and turbine trip occurred due to a spurious

high main steam flow indication.

Coastdown operations subsequently re-

sumed until November 21, when a second high steam flow trip occurred due

to crosstalk between protection channels during system maintenance / test-

ing.

After measures were implemented to control this interference, and

upon completion of routine shutdown maintenance, startup began on Novem-

ber 22. During power ascension, MFW pump problems again occurred, result-

ing in reduced power operation until November 27, when the plant was shut

down to repair the "A" MFW pump.

Power operations resumed on November

30 and continued until January 4, 1986, when the unit was shutdown for

the planned eight-week refueling / maintenance outage.

Refueling and maintenance activities included the core XIV fuel shuffle,

installation of a new permanent reactor cavity seal, steam generator

channel head decontamination and eddy current testing, an integrated leak

rate test, and several secondary system overhauls, upgrades or repairs.

In addition, modifications supporting equipment qualification, fire pro-

tection, seismic support upgrades, and the TMI Action Plan were imple-

mented.

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On February 26, while lifting the reactor core upper internals prior to

fuel offload, a single fuel element stuck to the internals.

As the in-

ternals assembly was being moved laterally, the fuel element hit the in-

side of the core barrel and fell onto two fuel elements in the core.

Its top end slid around the vessel and came to rest on the opposite side

of the core barrel.

Although individual fuel rods in the fuel element

were damaged, no radioactivity was released.

The dropped element was

safely recovered on March 2.

By the end of the assessment period, delays

associated with the dropped fuel element recovery, and problems with the

steam generator decontamination, reactor cavity seal and main turbine

low pressure rotors had extended the outage by several weeks.

2.

Inspection Activities

One NRC resident inspector was assigned during the entire assessment

period.

A second resident inspector was assigned on September 23, 1985.

The NRC inspection effort (both resident and region-based) for the one-

year assessment period totalled 1758 hours0.0203 days <br />0.488 hours <br />0.00291 weeks <br />6.68919e-4 months <br />.

There were two special inspections during the assessment period: (1) to

review the circumstances and corrective actions related to design change

control deficiencies (smoke detector removal) identified during Phase

I of the Process Computer Replacement; and (2) to review matters related

to component malfunctions and cross-wiring in the automatic Auxiliary

Feedwater Actuation Systems.

In addition, there were two NRC Team In-

spections: (1) An Emergency Preparedness Team observed the annual emer-

gency exercise on March 30, 1985; and (2) A radiation safety team in-

spection evaluated the radioactive materials transportation program.

An inspection and findings summary is appended to this report.

Fire

protection was not inspected in-depth as in prior years.

Consequently,

due to the lack of (1) readily apparent problems and (2) substantive team

inspection effort, fire protection is not evaluated this period.

3.

Supplementary SALP Functional Areas

This report discusses " Training and Qualification Effectiveness" and

" Assurance of Quality" as separate functional areas.

Although these

topics, in themselves, are assessed 'n the other functional areas through

their use as evaluation criteria, a synopsis is provided by each of these

two areas.

For example, quality assurance effectiveness has been as-

sessed on a day-to-day basis by resident inspectors and as an integral

aspect of specialist inspections.

Although quality work is the responsi-

bility of every. employee, one of the management tools to measure this

effectiveness is the use of quality assurance inspections and audits.

Other major factors that influence quality, such as involvement of first-

line supervision, safety committees, and worker attitudes, are discussed

in each functional area.

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II.

CRITERIA

Licensee performance is assessed in selected functional areas, depending on

whether the facility is in a construction, preoperational, or operating phase.

The functional areas normally represent areas significant to nuclear safety

and the environment, and are normal programmatic areas.

Special areas may

be added to highlight significant observations.

The following evaluation criteria were used to assess each functional area.

1.

Management involvement and control in assuring quality.

2.

Approach to resolution of technical issues from a safety standpoint.

3.

Responsiveness to NRC initiatives.

4.

Enforcement history.

5.

Reporting and analysis of reportable events.

6.

Stafting (including management).

7.

Training and qualification effectiveness.

Based upon the SALP Board assessment, each functional area evaluated is clas-

sified into one of three performance categories.

These are:

Category 1.

Reduced NRC attention may be appropriate.

Licensee management

attention and involvement are aggressive and oriented toward nuclear safety;

licensee resources are ample and effectively used so that a high level of

performance with respect to safety is being achieved.

Category 2.

Normal NRC attention should be maintained.

Licensee management

attention and involvement are evident and are concerned with nuclear safety;

licensee resources are adequate and reasonably effective so that satisfactory

performance with respect to safety is being achieved.

Category 3.

Both NRC and licensee attention should be increased.

Licensee

management attention or involvement is acceptable and considers nuclear safety,

but weaknesses are evident; licensee resources appear to be strained or not

effectively used such that minimally satisfactory performance with respect

to operational safety is being achieved.

The SALP Board also compared the licensee's performance in each functional

area during the last quarter of the assessment period to that during the en-

. tire period in order to determine the recent trend.

The trend categories used

by the SALP Board are as follows:

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Improving:

Licensee performance has generally improved over the last quarter

of the current SALP assessment period.

Consistent:

Licensee performance has remained essentially constant over the

last quarter of the current SALP assessment period.

Declining:

Licensee performance has generally declined over the last quarter

of the current SALP assessment period.

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III. SUMMARY OF RESULTS

A.

Facility Performance

CATEGORY LAST

CATEGORY THIS

PERIOD (9/1/83- PERIOD (3/1/85- RECENT

FUNCTIONAL AREA

2/28/85)

2/28/86)

TREND

1.

Plant Operations

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1

Consistent

2.

Radiological Controls

2

2

Consistent

3.

Maintenance & Modifications #

1

2

Consistent

4.

Surveillance

2

2

Consistent

5.

Emergency Preparedness

2

2

Consistent

6.

Security & Safeguards

1

1

Consistent

7.

Refueling /0utage Management

1

2.

No Basis

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8.

Assurance of Quality

2

2

Consistent

9.

Training and Qualification

2

Consistent

Effectiveness

10.

Licensing Activities

1

2

Declining

Modifications were previously addressed under Assurance of Quality.

Not previously addressed as a separate area.

B.

Overall Facility Evaluation

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In general, the licensee aggressively and thoroughly resolves matters

with immediate operational or safety significance.

The Security area

was particularly noteworthy in that, despite a long history of excellent

performance, there was a continuing aggressive effort to improve perform-

ance.

In other areas, however, there have been recurrent problems with

procedure adherence, personnel errors, attention to detail, and admini-

stration of routine activities.

Examples include numerous modification

control errors, significant ALARA flaws, and untimely submittals of

modification packages to the Plant.0perations Review Committee.

The

result has been satisfactory but generally lower SALP ratings.

To im-

prove overall performance, more effective management controls at all

levels are needed to assure that repetitive problems are identified and

corrected and that there is proper preplanning of work activities.

The

management attention to these activities that is evidenced in the Secur-

ity area is typical of that needed in other areas to avoid a further

decline in performance.

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IV.

PERFORMANCE ANALYSIS

A.

Plant Operations (425 hours0.00492 days <br />0.118 hours <br />7.027116e-4 weeks <br />1.617125e-4 months <br />, 24%)

1.

Analysis

This functional area encompasses operational activities, plant

housekeeping and fire protection, operator and staff performance,

review committee activities, event reporting, and corrective actions.

The previous SALP rated plant operations as Category 1.

In the last

SALP, strengths were noted in the quality of operator performance,

plant coordination of day-to-day evolutions, review committee ef-

fectiveness, and problem identification programs. Weaknesses were

noted in the operator requalification program, procedure adequacy

and compliance, and the scope and timeliness of corrective actions

for certain self-identified problems.

During the current SALP period, there were two region-based inspec-

tions of this area.

Plant operations were observed by the resident

inspectors throughout the period.

Operators carefully observed plant systems and conditions, and

promptly identified developing problems to management.

Through use

of the computer-enhanced maintenance reporting and tagging system,

operators efficiently tracked maintenance actions and implemented

system tagging.

Corrective actions were generally well planned and

ready for prompt implementation.

This team effort contributed to

there being no error-related plant shutdowns during the period.

The overall result was continuing effectiveness of the onsite team

of management, operators and support staff.

Control room operators were evaluated as having a professional ap-

proach to plant operations.

Although the age and small size of the

control room were noted as potential negative influences, plant

operators were observed to limit access to control panel areas,

maintain adequate control over extraneous noise, and perform their

duties effectively using readily available procedures, drawings,

and administrative aides.

Also, the licensee instituted a dress

code for plant operators.

Noteworthy housekeeping improvements were observed in the auxiliary

feedwater room and in the recovery of several contaminated areas

of the auxiliary building.

However, limited permanent and temporary

storage space onsite forces the licensee staff to accept occasional

clutter, and wet or soiled conditions.

Such was the case for the

auxiliary water treatment facility in the turbine hall and contami-

nated material storage in the spent fuel building lower level.

Upon

licensee identification of these degrading conditions, corrective

action was implemented.

A general upgrade of site facilities is

in progress.

Improved facilities for outage personnel have been

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provided.

Construction of new facilities is underway, primarily

for radioactive material processing and storage.

Such efforts,

along with a continued licensee initiative to recover and upgrade

remote areas such as the waste treatment building, RHR pit, and pipe

enclosures should result in further improvement of plant housekeeping.

<

The timeliness and thoroughness of corrective actions for some

problems identified in Plant Information Reports (PIRs) were iden-

tified in the previous SALP period as weaknesses.

The licensee

changed the PIR program to improve causal analysis and corrective

actions.

Staffing increases were approved, in part to help reduce

,

the PIR backlog.

Improvements were observed in the quality of PIR

reviews, and the PIR backlog was reduced. Many PIRs are, however,

returned for further corrective action and some (particularly those

related to fire barriers) involve recurrent problems.

Other recur-

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rent problems include late procedure reviews and self-identified

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radiological procedure violations.

Licensee efforts to decrease

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personnel errors and procedure-related problems have been partially

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effective.

The frequency of error-related operational events de-

clined, but the frequency of fire protection door control problems

rose (see LER trends cited in Section V).

Such recurrent problems

indicate lack of effective management involvement and follow through.

An evaluation of LER quality, using a sample of 10 LERs issued dur-

.

ing this assessment period, was made.

In general, the licensee's

LERs were found to be satisfactory.

The principal concerns iden-

tified were inconsistencies in subsection content between the

,

selected LERs, incomplete corrective action plans in some LERs, and

not addressing the possible consequences of events under different

initial conditions.

For instance, LER 85-29 reported a potential

failure dealing with loss of the semi-vital motor control center

(MCC-5).

The LER safety assessment concentrated on the plant indi-

cations and operator actions to mitigate the event but did not ad-

dress the more severe potential consequences.

Overall, however,

the quality of LERs has improved.

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Licensee onsite and offsite review committees have been effective

during this period.

The Plant Operations Review Committee has a

large workload including response to operational events, plant pro-

cedures, modifications, license changes and corrective actions for

Plant Information Reports.

The PORC accomplishes detailed and ef-

fective reviews.

PORC members are frank and inquisitive, and man-

agement is supportive of the open and detailed review conducted by

this committee.

Although the quality of PORC meeting minutes has

improved, they do not always reflect the details of PORC discussions

and often leave questions unanswered in the reader's mind.

A large

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number of multiple PORC reviews on individual topics and the length

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of PORC deliberations on certain reactive review efforts suggest

weaknesses in the staff work performed prior to PORC submittal.

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This unnecessarily involves PORC in details and can adversely affect

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the PORC's focus on the overall safety impact of the issue under

consideration.

(A weakness related to the drain on plant supervi-

,

sory activities created by lengthy PORC deliberations is described

in the Refueling and Outage Management Section of this report.)

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One PORC related violation was identified: PORC concurred in the

removal of Technical Specification required smoke detectors incident

to a design change.

This error was recognized by the licensee prior

to implementation of the change.

l

The offsite review committee (NRB) contributes effectively to safe

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plant operation.

Of particular note were the high quality and

timely NRB reviews of plant modifications and the assessment tech-

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niques used by NRB to evaluate staff performance annually.

In ad-

dition to routine audits, the NRB collects, trends and assesses

performance indicators such as audit and inspection report findings,

event reports, and nonconformance reports to measure staff perform-

r

ance.

A weakness identified by NRC concerned NRB involvement in

assuring the quality of audits conducted by the quality assurance

department.

NRB evaluation of audit scope, content, and findings

l

was noted as an area for improvement.

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No new operator license examinations were given during this period;

no NRC assessment of that aspect was made.

During this period, the

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licensee made progress on the upgrade program for licensed operator

requalification.

The upgrade and independent evaluation of certain

licensed operators continued throughout the period.

In January 1986,

the licensee began a revised requalification program which integrates

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training into the operator shift rotation schedule.

NRC review of

,

the preparations for implementation of this program identified no

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problems.

The program has improved the timeliness of operator

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feedback on procedural and hardware changes, and significantly in-

creases the training time to allow more discussion of the subjects

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covered.

Three violations were identified in the Plant Operations area.

None

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of these was a major violation.

However, one of the three was for

,

failure to adhere to procedures, which is a continuing problem noted

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in the previous SALP.

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In summary, although the licensee has improved each area of weakness

!

cited in the previous analysis, management attention is needed to

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further irrprove procedural compliance, LER quality, PORC efficiency,

I

and corrective action effectiveness.

Overall, the rating in plant

operations is weighted toward the operating staff's quality perform-

ance in several operationally significant aspects of the analysis.

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-2.

Conclusion

Rating:

Category 1.

Trend:

Consistent.

3.

Board Recommendation:

Licensee: None.

NRC:

None.

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B.

Radiological Controls (393 hours0.00455 days <br />0.109 hours <br />6.498016e-4 weeks <br />1.495365e-4 months <br />, 22%)

1.

Analysis

The previous SALP rated this area as Category 2.

Radiation control

. policy, procedures, and staffing were found to be program strengths,

while weaknesses were noted in management control and effectiveness

'in monitoring program compliance, in ALARA controls at the job

supervisor level, and in quality assurance (QA) for the radioactive

material transportation program.

During the previous assessment

period,.several violations were cited relating to a potential per-

sonnel overexposure during maintenance, and to QA problems in the

radwaste area.

A recent appraisal of the Health Physics program at the site found

that the overall program is a good one.

Weaknesses continued in

the ALARA program and in radwaste QA.

Program procedures are com-

prehensive and generally well written.

The Health Physics supervi-

sory staff is adequately experienced and dedicated, and shows in-

itiative in proposing and instituting measures to improve perform-

ance.

However, the recurrence of many minor, self-identified radio-

logical control procedure violations is indicative of ineffective

corrective actions in this area.

These incidents do not appear to

indicate any fundamental programmatic weakness, yet more extensive

training and accountability of workers and technicians is warranted.

The licensee has shown improvement in some aspects of radiological

controls.

This improvement was noted in the methods used in con-

tamination control and radiological surveillance during the 1986

outage.

These methods included innovative and effective techniques

such as subdivision of the radiation controls areas into autonomous

zones, and the use of closed-circuit television to monitor critical

areas. These methods were also effective in controlling the flow

of work and in keeping work areas generally clean and orderly.

Other improvements include selection and qualification of HP person-

nel and attention to the experience and capabilities of the person-

nel placed in charge of the work zones.

The Radiological Incident Reporting system instituted by the licen-

see is working.

Although management response to incidents identi-

fled by the system was initially inadequate, recently instituted

procedural changes appear to have led to improvement in this area.

These improvements include increased management attention to iden-

tify root causes and measures designed to minimize the chance of

recurrence of similar incidents.

One example of lack of such re-

sponse is an incident involving compacting of a' highly radioactive

drum in a manner that violated plant procedures and resulted in

internal and external exposure of workers, and extensive contamina-

tion of the work area.

This event displays a weakness in job pre-

planning and adherence to good health physics practices.

Management

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response in that case was insufficient.

Another incident identified

by the licensee is more recent and involved the installation of

hoses to a high integrity resin container for de-watering.

In that

incident, the couplings on the container and hook-up hoses did not

match.

Careful planning could have prevented this problem.

Fur-

thermore, the worker decided to remain in the high radiation area

while investigating the problem, rather than exiting to seek assist-

ance or to decide on the appropriate course of action.

As a result,

the worker exceeded his assigned exposure by a factor of about two.

Management response to this incident was more prompt and more com-

prehensive than in the case of the first example described.

Inci-

dents'such as those cited above are limited but recurrent instances

of poor judgement, mainly on the part of the Health Physics techni-

cians and the workers involved.

Weakness in the ALARA program was noted in previous SALPs and con-

tinues to be a problem.

Emphasis at the supervisory and technician

levels appears to focus mainly on keeping exposures within estab-

lished limits rather than minimizing them.

The same emphasis ap-

y pears to exist at management levels up through senior site and cor-

porate management.

Indications of this tendency are provided by

.

incidents such as those described above.

A common factor-in most

of these incidents appears to be the desire to "get the job done"

without sufficient regard for the radiological consequences.

An-

other indication of insufficient ALARA emphasis is the man-rem ex-

posure record of the station.

This record shows that the man-rem

exposures have been consistently much higher than those of the in-

dustry since at least 1979.

These exposures have also been consis-

tently higher than the licensee's own projections, particularly for

outage-related work.

Part of the reason for this relatively poor

exposure performance is ascribed to conditions peculiar to the sta-

tion.

The reactor system design is old and does not provide as much

component shielding as is found in more modern stations, thus lead-

ing to relatively high radiation fields in the work areas.

However,

a recent NRC appraisal of the ALARA program indicated that this

provides only a partial explanation for the poor ALARA performance.

The appraisal revealed serious weaknesses in the ALARA program at

all levels of management.

There are extensive and well written ALARA

procedures and policy statements, both at the station level and the

corporate level.

However, the ALARA program is essentially a paper

program, with poor implementation and oversight, particularly by-

corporate management.

Pre-job planning is frequently incomplete

and flawed, leading to unforeseen radiation exposures in attempts

to take remedial actions.

Pre-job planning is also frequently ill-

timed, leading to inadequate lead time for review of these estimates

by station personnel.

Short lead times also allow insufficient time

to consider all the ALARA measures that may be taken to reduce ex-

posures.

Furthermore, most high exposure outage jobs are performed

by non-station personnel, such as contractors, and control of the

number of people these contractors use and the man-hours expended

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in radiological areas appears to be poor.

There is extensive effort

expended in documenting job performance, analyzing the reasons for

exceeding goals, and proposing measures to improve performance.

1-

However, such efforts appear to receive inadequate management sup-

port.

Furthermore, most of the analyses do not clearly isolate and

identify the root causes of the problem.

Finally, the most dis-

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turbing aspect of this problem is that management action to take

effective corrective measures was not apparent.

With regard to Effluent Control and Environmental monitoring, in-

spections indicated that, while procedures are generally adequate

and are followed, several minor examples of deficient procedures

and instances of non-adherence to procedures were identified.

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Specifically, an Environmental Review Board failed to audit required

l

reports, calibration procedures for meteorological sensors were not

followed, and quality control samples were not sent to the vendor

!

laboratory.

Additionally, some records were found to be incomplete,

'

and documentation was sometimes insufficient to determine that dis-

crepant data had been reviewed.

All of these findings had minor

consequences but indicate weaknesses in the staff's implementation

of QA program requirements.

In areas directly affecting effluent

releases, such as radioactive releases, procedures and documentation

were complete and adequate for controlling and monitoring effluents,

and the QA program was sufficient to assure that all requirements

and specifications were met.

The implementation of the Radioactive Waste Handling Program (RWHP)

'

is generally adequate with regard to staffing and training of the

station' staff responsible for the mechanics of the program.

In

these areas, positions are well defined and identified relative to

responsibilities and authorities; and the training and qualification

program makes a positive contribution to performance of work with

few personnel errors.

Some procedures were found to have weaknesses,

but these were promptly addressed by the licensee.

The RWHP is also vulnerable relative to the assurance of quality.

In this area, quality assurance audits were found to lack sufficient

thoroughness; quality assurance personnel were not sufficiently

'

knowledgeable of shipping and radioactive waste disposal require-

ments; and~the specifications of 10 CFR 61 were not fully imple-

mer.ted by the quality assurance program.

As a result, errors on

the part of the radwaste handling department were not likely to be

caught by QA review of shipment activities.

For example, Iron-55

has been identified in the facility waste streams, but it was fre-

quently omitted from consideration in waste manifests and shipping

papers.

The repetitive omissions resulted in significant under-

estimation of activities in radwaste shipments, and were also in-

dicative of a breakdown in the responsibilities for assurance of

l

quality in radwaste shipments.

l

.

. . . -

-.

- - - . .

.. - - . _- . _ _ = _ _ - _ - - . _ -

.

14

In summary, the licensee has improved some health physics practices,

including better control and assignment of HP technicians, zone

coverage within the radiologically controlled areas, and followup

on self-identified radiation protection discrepancies.

However,

continuing problers in tha radwaste transportation and ALARA pro-

grams were not ,as significant weaknesses in this area.

Continued

increases in workload, contractor personnel onsite and personnel-

exposures during outages have emphasized the continuing poor ALARA

practices.

Althoegh improvements in some aspects of this functional

area were noted, the overall assessment was that radiological con-

trols performance nad declined since the previous SALP.

2.

Conclusion:

Rating:

Category 2.

Trend:

Consistent.

,

3.

Board Recommendation:

Licensee: Conduct a comprehensive management review of the ALARA

program and implement the changes necessary to achieve

an ef fective program.

NRC:

Continue normal inspection efforts eith special emphasis

on the implementation of the ALARA program.

1

(

F'

.

15

C.

Maintenance and Modifications (314 hours0.00363 days <br />0.0872 hours <br />5.191799e-4 weeks <br />1.19477e-4 months <br />, 18%)

1.

Analysis

'

The previous SALP rated maintenance as Category 1.

In a separate

analysis area, modification activities were rated as Category 2.

Documentation and trending of maintenance activities and the backlog

of plant maintenance work were previously noted as areas needing

improvement, and significant programmatic deficiencies in the design

change control area had resulted in escalated enforcement action.

During the current assessment period, one region-based inspection

reviewed the progress of NRC ordered design change control improve-

ments.

Two special inspections reviewed modification related prob-

lems in the auxiliary feedwater and fire detection systems, and the

resident inspectors reviewed maintenance activities throughout the

period.

The licensee has a strong preventive and corrective maintenance

program.

Automated tracking and scheduling of maintenance assists

in controlling the large nember of preventive maintenance (PM) tasks

performed.

Comprehensive and frequent program review and update

reflects management commitment to the PM program and has resulted

in a high degree of equipment reliability. One notable exception

during this period was the performance of the main feedwater system.

Several plant trips and shutdowns were directly related to main

feedwater system problems and the inability to isolate portions of

the system due to isolation valve leakage.

Had the feedwater system

isolation valves been repaired during the first system outage on

August 18, 1985, subsequent plant shutdowns for feedwater system

repairs would have been avoided.

The licensee recognized the im-

portance of feedwater system reliability as evidenced by the major

overhaul during the 1986 refueling outage.

The instrumentation and control (I&C) and maintenance departments

are manned by competent and motivated personnel.

Although a backlog

of maintenance activities remains, it is managed effectively by

prioritization and overtime, and the licensee has implemented or

approved new positions to improve the effectiveness of this organi-

zation.

The licensee is upgrading staff technical training, including

general system and technical speciality training.

Improved I&C

technician training in the Technical Specification operability as-

pects of maintenance and testing activities was implemented as a

result of an event in which a variable low pressure scram channel

of the reactor protection system was rendered inoperable during

.'

maintenance.

Based on generally high quality performance on other

maintenance activities, this maintenance error was judged to be an

isolated case.

- -

-

-

-

- - -

-

- . -

-

-

-

- -

-

-

r

.

.

16

During refueling outages, the plant staff is augmented by contractor

and utility workers in order to accomplish the large number of

maintenance activities. The licensee addresses the increased staf f

size by upgrading certain technicians to supervisory positions.

Repair activities during the 1986 outage were observed tc be pro-

perly conducted with the exception that a high pressure safety injec-

,

tion pump failed during post-maintenance testing.

The pump was not

reassembled properly because of personnel error and inadequate pro-

cedural update af ter pump modifications.

Significant pamp rework

was required as a result.

Also, several contractor performed vaive

repairs were repeated several times in order to achieve satisfactory

results.

These events appeared to be isolated cases in an otherwise

effective program.

Documentation of maintenance activities continued to be a weakness

during this period.

Poor documentation of rep & irs pievented accurate

determination of the cause of failure and contributed to the late

or incomplete submittal of several Licensee Event Reports (LERs

85-02, 05, 10).

Also, a violation involving several instances of

procedural noncompliance indicated inattention to detail in repair

activity control and recording. No equipment operability problems

were identified in these instances.

Three violations were identified in this area.

None of these was

major.

While multiple instances of modification control problems

were noted in one violation, these instances were not related.

As a result of previously identified weaknesses and hRC enforcement

action, the licensee implemented major changes to the modification

control program.

NRC review of modifications made during this SALP

period have identified significant improvement in the documentation

and control of design changes.

Nevertheless, continuing modifica-

tion control errors unnecessarily challenge the defense in depth

concept incorporated in the modification process.

NRC identified

discrepancies with testing, procedure updates, material issue,

technical specification changes, and documentation of field changes

for recent modifications point out the need for further improvement

in the implementation of plant modifications.

In one exarrple, ap-

proved rotests specified after emergency diesel generator air system

modifications would not have verified all aspects of system opera-

tion.

In summary, maintenance programs are ef fective overall and improve-

trent has been noted in the modification control program.

However,

maintenance errors involving procedural compliance were identified.

The backlog in and inadequate documentation of maintenance activi-

ties continued to be weaknesses.

Also, problems with the implemen-

tation of modifications were noted.

.

.

17

2.

Conclusion

Rating:

Category 2.

Trend:

Consistent.

3.

Recommendations:

Licensee: Provide effective management attention to the new modifi-

cation control process to assure that it is understood

and properly implemented at all levels.

NRC:

None.

i

l

t

l

I

.

.

18

D.

Surveillance (230 hours0.00266 days <br />0.0639 hours <br />3.80291e-4 weeks <br />8.7515e-5 months <br />, 13%)

1.

Analysis

Surveillance was rated Category 2 during the last SALP.

Inadequate

procedures and technician performance resulted in three events, one

of which received a mitigated escalated enforcement action.

In ad-

dition, weaknesses in the scheduling of surveillances and resolution

of containment leakrate. testing (CLRT) deficiencies were noted.

Surveillance was observed by resident inspectors throughout this

SALP period. The licensee continued the long term surveillance up-

grade program initiated during the previous period.

Procedural up-

grades and technician training were successful as evidenced by no

surveillance error-related events or violations being identified.

Several nuclear instrument problems were identified early in this

period.

Accelerated testing, troubleshooting and repairs were suc-

cessful in eliminating them.

inspector discussions with licensee technicians found them to be

competent, knowledgeable of procedures, and conscientious in the

implementation and evaluation of surveillance results.

The licensee's long term review of surveillance procedure adequacy

is ongoing and scheduled for completion in mid-1986.

Inadequacies

are still being identified as exemplified by the licensee's failure

to properly test 27 of 80 containment electrical penetrations be-

cause the test procedure listed an incorrect valve lineup.

In ad-

dition, several reported missed surveillances (see LER chain in

Section V of this report) occurred because procedures did not com-

prehensively cover all Technical Specification requirements.

Fur-

ther, there was minimal involvement of Quality Assurance in the

technical adequacy of surveillance procedures.

In addition, as

noted in Section V, 3 LERs addressed missed fire protection sur-

veillance tests due to personnel error.

One other problem involved

the licensee's failure to implement all aspects of a post-accident

systems integrity inspection commitment (LER 85-30).

Upon NRC

identification of this problem, the licensee fully implemented the

commitment.

During this period, an auxiliary feedwater initiation test failure

pointed out the need for more frequent exercise / testing of sticking

solenoid actuation valves as an action to prevent recurrence.

Be-

cause of licensee concerns about the acceptability of on-line test-

ing of this system, it took over ten months to develop and implement

the appropriate test procedure.

Then, when the test was run, a

similar initiation failure occurred.

Weekly testing thereafter

identified no further component failures.

l

.

.

/

~13

NRC inspection of previous CLRT activities identified weaknesses

including the quality of Type A test techniques and the responsive-

ness to previous NRC inspection findinge,.

The licensee made efforts

,

to formalize CLRT activities among its units and centralize the CLRT

'

,

program under a governing corporate level procedure.

NRC observa-

tion of CLRT activities shortly after the end of this assessment

i

period identified improved test performance. With regard to open

inspection findings, the licensee's approach was not fully respon-

sive.

The licensee response to the previous SALP indicated that

the open inspection items would be addressed in the last quarter

of 1985.

The licensee position submitted on December 23, 1985,

restated previous positions which did not resolve the existing dis-

crepancies with 10 CFR 50 Appendix J.

The licensee has a basically sound surveillance pregram which pro-

!

perly performs a large number of tests in a timely manner without

challenging safety systems.

There are, however, continuing problems

with surveillance procedures, QA of surveillance activities, imple-

mentation of commitments, and timeliness of corrective actions.

2.

Conclusion

Rating:

Category 2.

Trend:

Consistent.

3.

Board Recommendation

Licensce: Complete the ongoing surveillance upgrade program.

NRC

None.

,

i

_

_

_

_. . _ _

_ _ . . .

- . . _

._

,___m

. _ _ _ .._,. -

.

20

E.

Emergency Preparedness (166 hours0.00192 days <br />0.0461 hours <br />2.744709e-4 weeks <br />6.3163e-5 months <br />, 9%)

1.

Analysis

The previous SALP rated this area as Category 2.

There were three

j

significant deficiencies which were identified during the full-scale

)

emergency exercise in May 1984.

These deficiencies, involving in-

formation flow between the Control Room and Technical Support Centers

(TSC), delayed declaration of Emergency Action Levels and demonstra-

'

tion of technical support functions at the TSC, were addressed by

a Confirmatory Action letter (CAL 84-10) on June 5, 1984.

)

During this period, one NRC inspection was conducted to review

changes made to the Emergency Preparedness Program and to observe

the March 30, 1985 annual full-scale emergency exercise.

It war

found that the corrective actions described in CAL 84-10 had been

satisfactorily completed.

During the 1985 exercise, the licensee

demonstrated the new TSC which had been established within the

Emergency Operations Center (EOF).

Technical support activities

were adequately implemented except that the development of approved

emergency procedures was not demorstrated.

There were no majcr de-

ficiencies noted in the 1985 exercne; however, twenty minor defi-

ciencies were identified, and several of these problems were recur-

rent items from the previous exercise.

The licensee's onsite emergency preparedness staff consists of one

full time Emergency Planning Coordinator who is provided with emer-

gency preparedness activitiet support by corporate and contractor

personnel.

NRC observation of emergency exercise activities pon-

cluded that personnel were appropriately trained and qualified to

perform their emergency functions.

The licensee's performance

demonstrated that they could implement their Emergency Plan and

its implementing procedures adequately.

The licensee's multiple locations for command and <:ontrol and tech-

nical support functions provide independent assessment of emergency

activities and backup technical support.

However, redundant acti-

vities in these distant centers are often confused by delayed or

incorrect data, resulting in improper recomniendations or unnecessary

requests for clarification,

lhis vulnerability of errergency acti-

vities to good real-time data comunication emphasizes the need for

a hard-wired plant data transmission system.

In the interim, the

licensee has a dedicated data coordinator who responds to the emer-

gency response team paging system and manually inputs plant data

to the transmission network (NESS) available at the emergency oper-

ating centers.

Telecopiers are available to back up the NESS system.

Also, the State and utility emergency plans incorporate automatic

protective action recommendations (PARS) with the declaration of

each Emergency Action Level (EAL).

This makes event classification

and EAL declaration particularly important, and different because

'

'

'

'

j

.

'

,

,

.

.

/

1

'

-

.

l

,

21

,

,

f

"g

the class]fication may' carry with it inappropriate sheltering or

i

evacuation recommendations.

Resolution of these discrepancies re-

-

quires coordination at all emergency,' centers, which could either

'

delay event classification or result in overly conservative PARS.

s

,

~

'

No' actual events during this assessment period required the imple-

mentation of the Emergency Program.

Inspector observation of oper-

ational occurrences such as plant trips and a February 1986 dropped

fuel' element event identified appropriate operator response, prompt

2

'l

.

management support, and safe and conservatively planned recovery

activities.

In pEeparation for Hurricane Gloria in September 1985,

,

tne licensee chose to fully man the emergency facilities, with pro-

visions for extended implementa, tion of the emergency organization.

'

The< storm passed through the area without any significant damage

.

to plant systems.

No deficiencies in emergency plan activities were

noted by onsite N,RC observers.

'

,

In summary, thallicensee corrected some of the previously noted de-

ficiencies and satisfactorily implemented the site emergency plan

during the' annual exercise.

No emergency planning weaknesses were

identified during operational occurrences.

_

2.

Conclusion-

Rating:

Category 2.

Trend:

Consistent.

3.

Board Recommendation

Licensee: Complete the installation of the hard-wired data transmis-

sion system, and review the effectiveness of automatic

protective action recommendations.

NRC:

None.

,

H

e

,

- m

.~,

-

,

_ . _ _ _ _ _ ,, . , - - .,

,

y

_ . .

, ,

y,_,,

.

.

.

,

.

22

F.

Security and Safeguards (79 hours9.143519e-4 days <br />0.0219 hours <br />1.306217e-4 weeks <br />3.00595e-5 months <br />, 5%)

1.

Analysis

Previous SALP evaluations have identified consistently high perform-

ance in this area.

During this rating period, one routine physical

security inspection and one routine material control and accounting

inspection were performed by region-based inspectors.

Routine

resident inspections continued throughout the assessment period.

No violations were identified.

Management is involved in the physical security program and continues

to be supportive.

Resource planning continues to consider needs

for improving quality by self-inspection techniques and ensuring

comprehensive corporate audits.

These efforts, combined with a

positive management approach and clear, concise procedural controls,

contributed to error-free performance by the security organization.

As a result, during three consecutive rating periods, no violations

of NRC requirements have been identified.

The decision making pro-

cess for the security program, by management and supervisory per-

sonnel, is effective.

Records are well maintained and available.

Security improvements noted during this rating period included the

purchase of a new vehicle to enhance site perimeter patrols, in-

stallation of new protected area fencing, paving a perimeter access

road, purchase of additional security force shelters, completion

of renovation of the interior of the security building, development

of a slide presentation of security program features for use as a

training /information aid, and the expansion cf the drill program

in support of the Safeguards Contingency Plan.

A total of 180

drills were carried out by the security organization during CY 1985.

These improvements demonstrate the licensee's continuing support

of the program.

As a new initiative, the licennee is utilizing the NRC's Regulatory

Effectiveness Review Program generic findings from other licensed

sites to improve the effectiveness of its security program.

Im-

provements to barriers, detection aids, and duress procedures have

been implemented as a result.

The licensee maintains dedicated technicians for support of security

systems and equipment. The effectiveness of this is evidenced by

the fact that only one security event during this period involved

a hardware problem (four hardware-related problems were reported

during the previous period).

The problem caused the computer to

be off-line for only 21 minutes, during which time repairs were

effected.

Compensatory measures were effectively implemented and

the licensee's event report to the NRC was timely and comprehensive.

_ __.

.

.

-

..

,

.

.

.

.

23

,

Staffing of both proprietary and contract security positions was

effective.

Sufficient, well-trained and qualified supervisors and

security officers were assigned during the period.

Morale and pro-

,

fessional competence were observed to be high.

Also noteworthy was

the ability of security force members at all levels of the organi-

zation to describe their duties and responsibilities, in detail and

,

without hesitation.

This was done with enthusiasm and pride.

The licensee's consitment to continuously improve professional skills

via the use of drills and job knowledge critiques strengthens the

performance capability of the organization.

Additionally, the lic-

ensee provides funds for management /sepervisory attendance at pro-

fessional seminars and training courses.

There were two Security Plan changes submitted in accordance with

'

10 CFR 50.54(p) during this rating period.

The revisions were re-

viewed and considered acceptable.

The changes were adequately sum-

marized and appropriately marked on revised pages for clarity.

With regard to material control and accounting practices, the lic-

ensee was in compliance with NRC requirements.

Procedures and prac-

tices were adequate for the control of special nuclear material.

Records and reports were complete, well-maintained and available.

!

In summary, security and safeguards inspections by resident inspec-

tors and region-based specialists have identified exemplary programs.

Security continues to be a noteworthy licensee strength, because

of managocent support for program improvements, aggressive self

evaluation, and prompt and effective preventive / corrective actions.

2.

Conclusion

Rating:

Category 1.

Trend:

ConsistenL

.

3.

Board Recommendation

Licensce: None.

NRC:

None.

.

I

?

e

j

>

r

-,

,

-

-.4

-

..

.

- - -

,-

+- ,

.

- . ..

24

G.

Refueling and Outage Management (151 hours0.00175 days <br />0.0419 hours <br />2.496693e-4 weeks <br />5.74555e-5 months <br />, 9%)

1.

Analysis

Previous licensee performance in refueling and outage activities

has been Category 1.

During this period, a planned 8-week refueling

,

outage began on January 4, 1986.

By the end of the assessment

period, delays-in installation of a new permanent reactor cavity

seal, problems with decontamination of steam generator primary

channel heads, and recovery of a fuel assembly dropped during re-

fueling operations had extended the outage by approximately 25 days.

Refueling and outage activities were reviewed by the resident in-

spectors and a region-based project inspector, including outage

preparations and coordination, refueling operations, and recovery

after the February 26, 1986 dropped fuel element event.

The licensee maintained 24-hour per day management level coordina-

tors to follow outage activities and bring problems to management

attention.

Also, outage status meetings were held twice a day with

all departments and critical jobs represented.

The licensee's com-

-

puter-based outage planning program was effective in tracking the

details of job status,

Strong licensee commitment to the mainten-

ance and updating of this program was evident throughout the outage.

Consequently, it was readily recognized which critical path activi-

ties were experiencing problems such that additional attention could

be focused in that area.

Under this closer scrutiny, the allotted

,

time for some jobs was found to be incorrect.

In particular, under-

estimation of work package preparation, establishment of plant con-

ditions, and coordination and documentation of system turnover re-

quirements reflected inadequate pre planning of outage activities.

As a result of deadlines and commitments, several plant modifica-

tions were required to be implemented during this outage.

These

modifications included reactor vessel level indication, various

Appendix R improvements, seismic support upgrades, and equipment

environmental qualification replacements.

Although the licensee

has guidelines which require early submittal of plant design change

packages, only 8 of 32 modifications were ready for implementation

at the start of the outage.

In addition, the need for twenty other

'

modifications was identified during the outage.

Consequently, a

major effort involving considerable engineering and supervisory

effort was necessary, especially during the first month of the out-

age, to assure the appropriateness of pre-approval release of modi-

fication work packages and in the review and approval of the modi-

fications as they became ready.

,

.

-.

.,.,.r

.

. , . . . - , . . - .

c ..

-

,,y,,

, . - .

p

--.4-,

. ,,+.-

-.

-

.

.

,

.

25

Although no safety-significant discrepancies in design change imple-

,

mentation were noted as of the end of the assessment period, the

high volume of modifications implemented prior to completion of the

final design approval taxed those responsible for quality implemen-

tation of field installations.

,

Another negative aspect of the large expenditure of engineering and

supervisory talents in design change package preparation and review,

noted in Section C, was the diversion of these talents from their

-

normal line organizational functions during the outage.

Better pre-

job planning, supervision, and coordination may have reduced or al-

leviated such problems as were experienced with the steam generator

(SG) TV camera setup, SG decontamination, and high pressure safety

injection pump repair jobs.

In addition, more direct management /

supervisory effort to reduce job-related radiation exposure might

have reduced or eliminated the margin by which many outage jobs

exceeded the man-rem exposure goals as detailed in Section B.

The dropped fuel element on February 26, 1986 created a significant

perturbation of outage activities.

Recovery actions including

dropped element inspection and recovery, core component damage

evaluation and repairs, and re-analysis of the core reload pattern

excluding the damaged elements were promptly integrated into the

outage schedule.

The licensee's cautious and deliberate approach

to recovery action reflected a strong commitment to' plant safety

at the expense of the outage schedule.

However, the coordination

of preparations for recovery actions such as production and testing

of lift rigs could have been improved.

In two instances, the re-

covery efforts were delayed because lift rigs had not been prepared

in parallel with procedure preparation.

Overall, however, through-

out the recovery process, management priorities were properly di-

rected toward assuring the safety and quality of the recovery pro-

cedures and training, and the alertness of the recovery team.

In summary, although outage activities were carefully scheduled and

tracked, notable inadequacies in job pre planning and coordination

were identified.

Extraordinary supervisory efforts were required

to assure proper implementation of safety-related system modifica-

tions.

Those efforts challenged the level of quality assurance

normally provided by supervisory oversight.

2.

Conclusion

Rating:

Category 2.

Trend:

No Basis.

3.

Board Recommendations

Licensee: Commit additional attention to the pre planning of outage

activities, especially design changes.

NRC:

None.

.

..

.

_ __- _ -

. . -

. - .

-

-

_ _ _ _ _ _ _

.

.-

- - ,

-

.

.

,

.

26

H.

Assurance of Quality

1.

Analysis

During this assessment period, management involvement and control

in assuring quality is being considered as a separate functional

area in addition to being one of the evaluation criteria for the

other functional areas.

Consequently, this discussion is a synopsis

of the assessments relating to quality work conducted in other areas.

Licensee management emphasizes proper performance on the first try

and that quality is each individual's job.

Therefore, the QA or-

ganization is not looked upon as the central control for quality;

line management is.

However, for those individual errors which are

not picked up by supervisory oversight, management has other tools

to assure quality such as onsite (PORC) and offsite (NRB) review

committees, quality control (QC) inspections, and QA audits.

The

. success of this program is evident in the high quality performance

of individuals noted in selected aspects of the operations, main-

tenance, and security areas.

On the other hand, individual errors

which were not identified or corrected by quality assurance activi-

ties were also noted in the radiological controls, surveillance,

and modification areas.

PORC and NRB were noted to be effective in their assigned' functions;

however, these functions were notably reactive, and were not effec-

tive in preventing the recurrence of certain procedural and modifi-

cation-related problems.

QA/QC coverage of backfit and Betterment

Engineering projects was evident in the number of QA/QC findings

required to be dispositioned during the 1986 outage.

QC coverage

of maintenance was not as extensive.

Licensee improvement in QA/QC

involvement in operational activities in progress and in the rad-

waste transportation area was observed.

However, NRC identification

of ongoing problems with personnel errors, procedural adequacy,

surveillance scheduling, and radwaste processing and shipment indi-

cate a need for more effective self-evaluation.

It was also noted

in several areas that the corrective actions for NRC and self-iden-

tified problems were not always effective in preventing recurrence.

Control of fire barriers, missed surveillances, and inadequate ALARA

controls were examples.

QA audited activities in accordance with department schedules.

NRC

review of audit reports found them to be generally effective. With

the exception of one environmental audit program which omitted re-

quired document review in the audit scope, no audit program defi-

ciencies were identified.

Nonetheless, the NRC noted that improve-

ment in management involvement in audit scope, findings, and cor-

rective action promptness was needed to improve the quality and

effectiveness of the self-evaluation process.

.

_

l

'

.

,

27

In summary, the licensee performs many activities very well, pri-

marily as a result of good individual and supervisory efforts.

The

review committees were effective from a reactive perspective and,

to the extent employed, QA audits and inspections were satisfactory.

However, many minor problems were identified and several of these

continued throughout the assessment period without effective cor-

rective action.

Management involvement in preventing problems, and

assuring quality in all activities was noted as an area for improve-

ment.

-2.

Conclusion

'

Rating:

Category 2.

Trend:

Consistent

3.

Board Recommendations

Licensee: Reevaluate the effectiveness of systems for self-

identification and resolution of problems.

NRC:

None.

- -

-

_ ,.

-

.

.

.

,

.

28

I.

Training and Qualification Effectiveness

1.

Analysis

During this assessment period, Training and Qualification Effective-

ness is being considered as a separate functional area for the first

time. Training and qualification effectiveness continues to be an

evaluation criterion for each functional area.

,

.The various aspects of this functional area have been considered

and discussed as an integral part of other functional areas and the

respective inspection hours have been included in each one.

Conse-

quently, this discussion is a synopsis of the assessments related

to training conducted in other areas.

Training effectiveness has

been measured primarily by the observed performance of licensee

personnel and, to a lesser degree, as a review of program adequacy.

The discussion below addresses three principal areas: licensed

operator training, non-licensed staff training, and the status of

INPO training accreditation.

The licensee's commitment to comprehensive and effective training

programs at all organizational levels was evident in the ambitious

program of training development and accreditation ongoing throughout

this assessment period.

At the end of the period, though no train-

ing programs had been accredited by INP0, the licensee had reas-

4

sessed the program goals and milestones to establish a " ready for

accreditation" status in all operator, staff, and technician-pro-

-

grams before the end of 1986.

No new operator license examinations were given during this period.

The licensee continued to implement the upgraded licensed operator

requalification program committed to as a result of significant

weaknesses identified as a result of NRC audits during the previous

period.

In January 1986, a new requalification program was initi-

ated, including requalification as an integral part of the normal

operator shift rotational schedule.

NRC review of the licensed

operator upgrade program and the preparations for the new requali-

fication program identified satisfactory completion of the licen-

see's commitmerits.

A site-specific simulator has been installed

and should be operational in mid-1986.

.The licensee relies heavily on departmental on-the-job training to

establish and maintain personnel technical qualification. General

employee training (GET) provides safety, security, and health

physics training.

The security department was particularly noted

as having an effective training orogram.

Overall, the quality of

operations, maintenance, and surveillance activities reflects

training strengths in these areas. Weaknesses were identified in

some functional areas such as: I&C technician understanding of

Technical Specifications (maintenance); engineer understanding of

-

w

m

t-

=r

-

w,

w r w-

w -

w-

ww

ey

pe-

_

.

.

,

.

29

design change control procedures (modifications); inattentiveness

of the licensee's staff to minimizing radiation exposures, and

quality control inspector knowledge of radwaste transportation;

(radiological controls); and general knowledge of the control of

fire barriers (plant operations). These weaknesses indicate the

need for improved training in these areas.

Another problem identified during this period related to weaknesses

in licensee control over the examination process for GET. The fail-

ure to establish formal examination controls during GET testing al-

lowed the occurrence of an incident involving talking between ex-

aminees during a GET exam.

The licensee responded adequately to

this event by implementing more comprehensive examination controls

for all training programs.

In summary, the minimal number of personnel-error-related operational

events reflects positively on the effectiveness of operating staff

training.

Likewise, strong licensee performance in security and

maintenance are due in part to the effectiveness of training in these

areas.

It was also noted, however, that recurrent weaknesses in

the ALARA, modification control and fire protection programs result

from personnel errors and misunderstanding of program requirements.

These reflect negatively on the quality of training in these areas.

2.

Conclusion

Rating:

Category 2.

Trend:

Consistent.

3.

Board Recommendations.

Licensee: Reorient technical training programs to address weaknesses

identified in the functional areas.

NRC:

None.

,

,.

_ . - , , - , - , . ,

- - - - ,

, . . . -

- . , . .

'

.

,

30

J.

Licensing Activities

1.

Analysis

The basis of this appraisal was the licensee's performance in sup-

port of licensing actions that were either completed or active dur-

ing the current rating period.

These activities consisted of

amendment requests, exemption requests, responses to generic letters,

TMI items, SEP and ISAP topics, and related actions.

Licensing activity during the SALP period has been at a very high

level.

Although several licensing actions have been deferred for

resolution under the Integrated Safety Assessment Program (ISAP),

twice the number of licensing actions have been completed during

this 12-month rating period than were completed during the previous

18-month SALP period.

In addition to the routine actions, major

activities completed or ongoing include fuel reload (Cycle 14), steam

generator tube sleeving, the voluntary ISAP initiative, environmental

qualification modifications, exemptions for fire protection require-

ments, and the requirements for an updated Facility Description and

-

Safety Analysis (FDSA).

At the start of the SALP rating period,

there were 75 active licensing actions.

During the rating period,

50 actions were completed and 29 new actions were added.

Thus, at

the end of the rating period, 54 active actions remain.

The specific

licensing activities reviewed are listed in Section V.E of this re-

port.

In resolving technical issues, the licensee has exhibited a good

understanding of licensing issues and has generally employed a con-

servative safety approach.

The licensee's applications or submittals

were generally timely and acceptable resolutions were generally pro-

posed.

For example, the licensee's application for relief from some

requirements for inservice inspection of reactor coolant pumps was

well prepared and exhibited a conscientious effort to comply with

the regulations. However, there have been some instances where the

licensee's resolution of technical issues and responsiveness have

been poor.

Examples are: submittal of information concerning the

reliability of the Auxiliary Feedwater System, and in support of

Technical Specifications for degraded grid protection, facility

overtime, RETS and STS conversion.

While the licensee's management has been notably involved in major

licensing issues, there have been occasions when incomplete or un-

timely submittals have caused the staff to request improved manage-

ment oversight.

Notable examples include the Cycle 14 reload and

steam generator tube sleeving license amendment applications.

The

Cycle 14 reload application, dated December 11, 1985, lacked the

necessary technical information which was subsequently provided on

January 16, 1986.

Similarly, the steam generator sleeving applica-

tion was received December 6, 1985, but the technical justification

(sleeving report) was not provided until January 7, 1986.

The un-

-

.

i

31

timeliness of the supporting technical material for the above ap-

,

plications created a significant burden on the staff to complete

the required licensing reviews to support the scheduled startup date

'

of March 4, 1986.

Similar examples of untimely submittals of exemption requests for

issues being addressed under ISAP have occurred near the end of this

rating period.

Notable examples include the schedular exemption

requests for the fire protection modifications in the switchgear room

(March 7, 1986) and for Appendix J (March 12,1986).

Both examples

reflect cases where approval / denial of these exemption requests were

outage related issues yet the submittal of the requests occurred

well into the outage.

We believe that the above examples demonstrate that the performance

and management oversight of licensing activities were declining

during the end of the rating period and that it does not appear to

be at the level of previous rating periods.

There also appears to be a tendency on the licensee's part to declare

a position on issues without providing the follow-up needed to assure

appropriate licensing actions are formulated to address the issue.

In particular, Appendix R, environmental qualification (feed and

bleed), and other exemptions related to issues being considered under

ISAP were filed close to the regulatory deadlines with significant

technical issues yet to be resolved.

Although the licensee had pre-

viously addressed these areas, they had not aggressively followed

through to assure the acceptability of their positions.

In conclusion, management attention and involvement with matters

of nuclear safety are evident, but there also is evidence that the

quality of the licensing activities at the Haddam Neck Plant has

decreased.

During this rating period there were instances when

amendment applications were either incomplete or untimely, and when

follow-up activities were delayed.

Requests for extension of sub-

mittal dates were common, reflecting an inadequate level of pre-

planning.

2.

Conclusion

Rating:

Category 2.

Trend:

Declining.

3.

Board Recommendations

Licensee: Take action to assure that licensing submittals are ade-

quately pre planned, comprehensive and reflect considera-

tion for regulatory deadlines.

Aggressively pursue each

open item to closure.

NRC:

None.

i

'

-

.

32

V.

SUPPORTING DATA AND SUMMARIES

A.

Investigation and Allegation Review

,

Two allegations were received during this assessment period.

One alleged

that the licensee exceeded Technical Specification (TS) rod insertion

limits.

No evidence was found to substantiate this allegation.

The

second allegation concerned an incident involving two examinees discuss-

ing test material during a General Employee Training (GET) exam.

This

allegation was substantiated.

Although this was shown to be an isolated

case, a lack of clear instructions for exam conduct and an inadequate

testing environment were found by the licensee to need corrective action.

The licensee upgraded their examination administrative controls to cor-

rect the deficiency and close out the allegation.

The individuals in-

volved passed a subsequent reexamination.

B.

Escalated Enforcement Actions

1.

Civil Penalties

There were no civil penalties issued during this assessment period.

2.

Orders

A memorandum and order, issued on November 20, 1985, granted an ex-

tension from the November 30, 1985, deadline for environmental

qualification of electrical equipment.

The deadline was extended

(

to January 4, 1986.

Modifications needed to fully qualify the ex-

empted equipment were implemented during the January-April,1986

refueling outage.

3.

Confirmatory Action Letters

There were no confirmatory action letters issued during this as-

sessment period.

C.

Management Conferences

1.

On March 25, 1985, an enforcement conference was held at the NRC

Region I office to discuss Reactor Protection System (RPS) Loss of

Flow trip channel problems and associated surveillance and proce-

dural reviews.

2.

On October 31, 1985, a management meeting was held at the NRC Region

I office to discuss the causal factors and corrective actions for

auxiliary feedwater system wiring deficiencies.

.

.

33

D.

Licensee Event Reports

1.

Tabular Listino

Type of Events:

A.

Personnel Errors

14

B.

Design / Man./Const./ Install

5

C.

External Cause

0

D.

Defective Procedure

2

E.

Component Failure

14

X.

Other

2

Total

37

LERs Reviewed

LER No. 85-03 to 86-09

2.

Causal Analysis (Review Period 3/1/83 - 2/28/86)

Six sets of common mode events were identfied:

LERs 85-14, 85-18, 85-22, 85-27 and 86-01 reported fire door

a.

control problems caused by personnel errors.

b.

LERs 85-12, 85-23 and 86-07 reported missed fire protection

system surveillance tests due to personnel errors.

c.

LERs 85-04, 84-12 and 86-06 report failures of containment

penetration local leak rate tests during three consecutive

surveillance cycles.

d.

LERs 84-28 and 86-02 reported main steam safety valve setpoint

drift problems.

e.

LERs 85-5 and 85-24 reported auxiliary feedwater system actu-

ation problems caused by sticking solenoid-operated actuation

valves.

f.

LERs 84-10 and 86-04 reported problems with operability of the

low pressure overpressure protection system.

There was a small increase in the percentage (38% to 43%) of per-

sonnel/ procedural error-related events since the previous assessment

and a high level of component failures.

-.

.

-

.

--

- _ -

>

.

.

,

.

,

34

i

!

E.

Operating Reactor Licensing Actions

1.

Schedular Extensions Granted

March 28, 1985; Extended the deadline for environmental qualifica-

.

tion of electrical equipment to Ncvember 30, 1985.

.

August 26, 1985; Extended the date of compliance with commission

order (dated June 12, 1984) upgrading the Emergency Operating

Procedures (E0P) at the Haddam Neck Plant to September 1, 1986.

,

2.

Reliefs Granted

,

June 10, 1985; Relief granted from requirements of Section XI of

ASME Boiler and Pressure Vessel Code for volumetric examination

r

of reactor coolant pump casing welds.

3.

Exemptions Granted

April 11, 1985; Granted a six (6) month exemption from 10 CFR 50.71(e) requirements updating the Facility Design and Safety

Analysis (FDSA).

.

November 22, 1985; Conditionally extended the April 11, 1985 (FDSA

l

upgrade) to June 30, 1987, provided specified milestone FDSA sub-

mittals are met.

'

l

4.

License Amendments Issued

Amendment No. 62 issued on April 24, 1985, revised Technical Speci-

!

fications to change the Power Dependent Insertion Limits curve to

[

allow greater flexibility in plant operations when reducing or in-

,

l

creasing power.

!

Amendment No. 63 issued on July 1, 1985, changed the completion date

'

,

l

for Item III.D.3.4, Control Room Habitability, as specified in the

commission's March 14, 1983, Confirmatory Order.

Amendment No. 64, issued on August 12, 1985, deleted Technical

Specification Environmental Qualification (EQ) requirements as cur-

rent EQ and schedular requirements were incorporated into 10 CFR 50.49.

L

Amendment No. 65 issued on September 3, 1985, revised Technical

l

Specifications by deleting the logic requirement of the Pressurizer

l

Low Water Level for the Safety Injection Trip.

l

Amendment No. 66 issued on September 3, 1985, modified Technical

Specifications to add new Limiting Conditions for Operations and

i

l

Surveillance requirements for Post-Accident Instrumentation.

!

!

- . -

.

.

. _.

- - -

- - - -

.

-. - - . - - .--

'

.

.

35

,

Amendment No. 67 issued on September 3, 1985, modified Technical

Specifications to change discharge pressure requirements for Emer-

gency Core Cooling System (ECCS) pumps.

Amendment No. 68 issued on September 5, 1985, approved Radiological

Effluent Technical Specifications (RETS) which incorporated the re-

quirements of Appendix I to 10 CFR 50 and deleted Technical Speci-

fication Appendix B, Environmental Technical Specifications.

Amendment No. 69 issued on October 16, 1985, modified Technical

Specifications to restrict the volume of flammable liquids in the

control room to no greater than one pint.

Amendment No. 70 issued on October 16, 1985, revised Technical

Specifications to update the pressure and temperature limit curves

for hydrostatic and leap. rate testing and for heatup and cooldown

rates.

Amendment No. 71 issued on December 10, 1985, revised Technical

Specifications to include restrictions on the excessive use of

facility staff overtime.

Amendment No. 72 issued on February 19, 1986, revised Technical

Specifications to allow testing of normally closed, non-automatic

isolation valves that are part of the Post Accident Sampling System

(PASS).

..

.

.

,

.

TABLE 1

TABULAR LISTING 0F LERs BY FUNCTIONAL AREA

HADDAM NECK PLANT

AREA

NUMBER /CAUSE CODE

TOTAL

A.

Plant Operations

7A

3B

6E

2X

18

B.

Radiological Controls

none

C.

Maintena.;te & Modifications

2A

2

D.

Surveillance

5A

2D

8E

15

E.

Emergency Preparedness

none

F.

Security and Safeguards

none

G.

Refueling and Outage Management

none

H.

Quality Assurance

none

I.

Training

none

J.

Licensing Activities

28

2

Totals

14A 5B

2D

14E 2X

37

Cause Codes

A - Personnel Error

B - Design, Manufacturing, Construction, or Installation Error

C - External Cause

D - Defective Procedures

E - Component Failure

X - Other

--

-- _

.

- -

-

-

-

-

. _. -

.

..

..

.

. . -

-

. . -

-

- - - - - .. __-

.

-

.

, .

TABLE 2

'

LER SYN 0PSIS

HADDAM NECK PLANT

LER No.

Summary Description

85-3

Nonconservative Loss of Flow Setpoint

85-4

NIS Overpower Setpoint Drift

85-5

Failure of Auto AFW Flow Valves to Open

85-6

Feed. Pump Suction Pipe Rupture

~

85-7

Plant Trip due to Feedwater Recirculation Valve

Failed to Open

1

j

-85-8

Cable Vault Ventilation System Inoperable

85-9

. Inoperable Fire Door

85-10

Service Water M0V Failure

.85-11

Multiple Dropped Control Rods 85-12

Failure to Perform Fire Detection Surveillance

'

85-13

Misaligned Rod Analysis

85-14

Inoperable Fire Door

Spurious Load Runback

85-15

-

85-16

NIS Dropped Rod Setpoint Drift

85-17

Post LOCA Release Paths Outside Containment

85-18

Inoperable Fire Door

-85-19

Spurious Load Runback

p

85-20

Potential Unauthorized Access to a High Radiation Area

,

85-21

Cable Spreading Area Fire Barrier Problems

85-22

Inoperable Fire Barrier

85-23

Missed Fire Protection Surveillance Test

,

4

.

1

w

s

e -

evw-,-

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-

w,-

,-ww

e-

r-

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--

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,r-,-

wm- . , - .w

--

- - - -

-,e

-ns

.

- . ,

,

T-2-2

.

LER No.

Summary Description

85-24

AFW Initiation 50V Failure

85-25

Unplanned Gaseous Release-

85-26

Partial Loss of Variable Low Pressure Scram Protection

85-27

Fire Barrier Penetrations

85-28

High Steam Flow Reactor Trips

85-29

More Probable Loss of MCC 5

85-30

Systems Integrity Inspection Missed

86-01

Inoperable Fire Doors

86-02

Main Steam Safety Valve Failures

86-03

Category C-3 Steam Generator Tube Inspection

86-04

Low Pressure Over Pressure Protection System Malfunction

86-05

Inoperable Switchgear Halon System

86-06

Containment Local Leak Rate Failures

86-07

Missed Fire Protection Surveillance

86-08

Improperly Tested Containment Penetrations

86-09

. Inadequate Service Water Flood Barriers

.

.,

.

.

TABLE 3

INSPECTION HOURS SUMMARY

HADDAM NECK PLANT

HOURS

% OF TIME

A.

Plant Operations . . . . . . . .

425

24

...

B.

Radiological Controls

393

22

.........

C.

Maintenance & Modifications

314

18

......

0.

Surveillance . . . . . . . . . . . . . .

230

13

E.

Emergency Preparedness . . . . . . . . .

166

9

F.

Security and Safeguards

79

5

........

G.

Refueling & Outage Management

151

9

.....

H.

Quality Assurance

-

-

...........

I.

Training . . . . . . . . . . . . . . . .

-

-

J.

Licensing Activities . . . . . . . . . .

-

-

Total

1758

100

Note:

Allocations of Inspection Hours vs. Functional Areas are approximations

based on inspection report data.

The Quality Assurance and Training

analyses are a synopsis of the evaluations of Quality Assurance and Train-

ing rating criteria in each functional area.

Consequently, inspection hours

for Quality Assurance and Training are included in the other respective

areas.

_

.. . - - - - -

. . - -

, _ _ . . . . .

_._

.

.

. . . . . . _ _ . _ - . . . _ . .

.

._

m

.- _. . _

-

.

,

'.,%

d

TABLE 4

-

ENFORCEMENT SUMMARY

HADDAM NECK PLANT

,

Severity Levels

FilNCTIONAL AREAS

I -II

III

IV V DEV

Total

A.

Plant Operations

3

3

.

B.

Radiological Controls

2

1

3

C.

Maintenance & Modifications

1

2

3

D.

Surveillance

E.

Emergency Preparedness

.

F.

Security Safeguards

,

'

G.

Refueling & Outage Management

H.

Quality Assurance

I.

Training

J.

Licensing Activities

.

Totals by Severity Level

6

3

9

.

A

1

-er.-

- - , - - , - , , _ , . -

. ~ , . , - - - , . - - - = - - - - , - ~ - -

,

--

-, -

,- -

w---

-- , - ,

, - - . , -

~ , _ ,

-

,

_

I

-

.

I

,

TABLE 5

ENFORCEMENT DATA

HADDAM NECK PLANT

Inspection-

Inspection

Severity Functional

Report No.

Date

Level

Area

Violation

85-08

3/15-29/85

V

B~

Inadequate scope of environmental

audit program.

85-09

4/8-12/85

IV

B

Failure to perform receipt in-

spection of Radwaste QA systems

and failure of PORC to review

a Radwaste processing procedure

85-15

6/14-26/85

IV

C

Inadequate design change review

such that a TS change was missed.

85-15

6/14-26/85

IV

A

Onsite review committee failure

to identify that a required TS

change was missed.

85-21

10/16-12/02/85

IV

A

Failure to follow procedures

(multiple instances).

85-21

10/16-12/02/85

IV

A

Inadequate corrective action for

previous violations.

86-01

1/9-2/6/85

V

C

Inadequate processing of modifi-

cation field changes.

86-01

1/9-2/6/86

V

C

Inadequate test plan for a plant

modification.

86-02

2/10-14/86

IV

B

Failure to compact radwaste in

accordance with an approved

procedure.

'

.

.,

-

.

TABLE 6

INSPECTION REPORT ACTIVITIES

HADDAM NECK PLANT

Inspection

Inspection

Areas

Report No.

Hours

Inspected

85-04

96

Radiological Controls

85-05

8

Management Meeting (Surveillance)

85-06

166

Emergency Preparedness

85-07

89

Routine Resident

85-08

54

Radiological Controls

85-09-

144

Radiological Controls

85-10

10

Management Meeting (Training)

85-11

66

Routine Resident

85-12

25

Security

85-13

137

Routine Resident

85-14

cancelled

85-15

30

Special Resident - (Design Change Control)

85-16

50

Fire Protection

85-17

36

Design Change Control

85-18

80

Requalification Program

85-19

99

Routine Resident

85-20

27

Special Resident (Auxiliary Feedwater)

85-21

152

Routine Resident

85-22

12

Management Meeting (Auxiliary Feedwater)

85-23-

19

_ Security

85-24

29

Chemistry

,

.

,

T-6-2

Inspection

Inspection

Areas

Report No.

Hours

Inspected

85-25

113

Routine Resident

86-01

206

Routine Resident

86-02

70

Radiological Control

.

86-05

40

Quality Assurance

,

1

,

'

l

-

.

.

,

1

s-

,

TABLE 7

PLANT SHUTDOWNS

HADDAM NECK PLANT

Shutdown Period

Description

Cause

March 12, 1985

Scram from 50% power.

High pressurizer Random Equipment fail-

pressure trip due to rapid plant load

ures

reduction as a resut of a loss of feed-

water flow to steam generators, which

was caused by a broken control air lire

to a feedwater recirculation valve.

A

main condensate pump motor short pre-

viously caused a load reduction to 50%

power.

March 16, 1985

Manual scram due to a main feedwater

Equipment Failure

pipe rupture.

The reheater drain pump (design-related)

flow control valve directed flow

against the pipe wall causing signifi-

cant erosion of the pipe.

May 16, 1985

Manual scram due to two dropped con-

Equipment Failure

trol rods.

(design-related)

August 18, 1985

Shutdown to replace a main feedwater

Equipment Failure

pump seal (pump isolation valve leakage

forced a shutdown rather than a power

reduction).

November 10, 1985

Scram due to spurious high main steam

Both events were caused

flow signals.

by a design deficiency /

abnormal operating

November 21, 1985

Scram due to spurious high main steam

conditions -- lower

flow signals.

margin to the trip

setpoint during coast-

down operation allowed

existing inter-channel

interference to actu-

ate the reactor pro-

tection system (de-

sign-related).

November 27, 1985

Shutdown to replace main feedwater

Equioment Failure

pump rotating assembly (pump isolation (maintenance planning-

valve leakage forced a shutdown rather related)

than a power reduction).

.

'

.

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1

ENCLOSURE 3

.

,

.

NORTHEAST UTILITIES

c,eme,& omces . smen som ee~n cemnecocut

T

P O BOX 270

. . . . . .

. . . .

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. . . . . . . . . . ~ . .

.

H ARTFORc CONNECTICUT Of141-0270

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!!.[*.h U..'.'.C'. [ ~,;

(203) 66s-s000

March 13,1986

Docket No. 50-213

50-245

50-336

Bl1979

Dr. Thomas E. Murley

Regional Administrator

Region i

U.S. Nuclear Regulatory Commission

631 Park Avenue

King of Prussia, PA 19406

Gentlemen:

Haddam Neck Plant

Millstone Nuclear Power Station, Unit Nos. I and 2

Svstematic Assessment of Licensee Performance

The SALP Board Reports (I) for the 18-month period ending February 28,1985,

for Haddam Neck, Millstone Unit No.1, and Millstone Unit No. 2 were issued on

May 20,1985. After a meeting between members of the Staff, Connecticut

Yankee Atomic Power Company (CYAPCO), and Northeast Nuclear Energy

Company (2)(NNECO) on June 4, 1985, Northeast Utilities (NU) submitted a

response

to the SALP Board recommendations for each of the individual

evaluation categories.

The purpose of this letter is to provide an update on the status of the

implementation of the corrective actions discussed in our July 5,

1985

correspondence. Items which were completed as of the July 5,1985 response are

not discussed in this letter. Attachment I to this letter contains the status of

the corrective actions related to the Haddam Neck unit which were incomplete

as of July 5,1985. The status of the corrective actions for Millstone Unit No. I

and Millstone Unit No. 2 are contained in Attachments 2 and 3, respectively.

(I)

T. E. Murley letter to J. F. Opeka, Systematic Assessment of Licensee

Performance (SALP), dated May 20, 1985.

(2)

J. F. Opeka letter to T. E. Murley, Systematic Assessment of Licensee

Performance, dated July 5,1985.

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We are again taking this opportunity to offer some additional observations on our

level of performance during the past year. In particular, we note that Northeast

Utilities executive management is active in numerous industry initiatives, having

made presentations at public meetings before the Commission as well as

participating in meetings with senior Staff management.

NU management

personnel are active in, and in many instances chair, various industry groups

addressing a wide range of nuclear issues.

Provided as Attachment 4 is a summary description of some of our attempts to

further improve the quality of the regulatory process by previding the regulators

with a continuing opportunity to become more f amiliar with our plants,

procedures, and personnel.

We trust that the actions presented in the attachments for addressing tne

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concerns of the Board will be useful in subsequent SALP evaluations. Feel free

to contact us if any questions arise on these matters.

Very truly yours,

,

CONNECTICUT YANKEE ATOMIC POTER COMPANY

NORTHEAST NUCLEAR ENERGY COMPANY

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3 p f peka

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Senior Vice President

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By: W. F. Fee

Executive Vice President

cc:

C. I. Grimes

A. C. Thadani

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Docket No. %-213

Bf1979

Attachment 1

Connecticut Yankee Atomic Power Company

Haddam Neck Plant

Updated Response to SALP Report

.

March,1986

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Functional Area: PLANT OPER ATIONS

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Board Recommendations:

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(A)

Improve the quality and aggressiveness of self appraisal

(B)

Continue emphasis on operator requalification

(C)

Continue initiatives to improve procedural review

(D)

Assess the adequacy and timeliness of PIR/CR disposition

UPDATE:

_

(A)

Increased management concern for self appraisal and self identification

programs has resulted in an upgrading of several existing programs.

d

The Plant Information Reports (PIR) system is undergoing prodedural

changes to place more emphasis on root cause analysis and corrective

action. The improvements in the analysis of cause should make the PIR a

more effective mechanism.

The Nonconformance Control Reporting system is functionally sound, but

at times a backich exists due to overall workload. Quality Assurance (QA)

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reviewers have b en instructed to put greater emphasis on ensuring that

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cause and corrective actions are adequately addressed.

The QA< audits are becoming more performance oriented. For example,

technical specialists are used on QA audit teams, an engineering assurance

function in the QA branch is being developed during the first quarter of

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1986, and the use of QA surveillances to review field activities has been

increased.

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The Beneficial Suggestion program has been very successful, with

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employees making many excellent suggestions for improvement on a wide

variety of topics. This is a unified system which includes Housekeeping,

ALAR A/ Radiological Safety, Fire Safety, and Personnel / Industrial Safety.

An evaluation of required resources to handle the large quantity of

suggestions wil: 50 performed af ter the 1986 refueling cutage.

The RaWe f cX Incide5t Report procedure has been upgraded and includes

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a dese.jp xa -

he responsibility of the individuals involved in preparing

the repm I, the athods of filing the report, and the ac*. ions to be taken..

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The Station Housekeeping and inspection Program was expanded to include

department heads performing periodic inspectiorc. ~

(B)

The Connecticut Yankee Plant Reference Simulator officially began

" Customer Factory Acceptance Testing" at the Link Facility in Silver .

Spring, MD on August 5,1985. The trainer has since been delivered and its

installation recently completed. Reverification testing is expected to be

completed by the end of March,1986.

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(C)

Improvements in procedural review and adherence are continuing.

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method currently in use at the Millstone site involving management review

and reissue of appropriate standing memos to station personnel as a

reminder of the importance of following procedures and, where required,

initiating changes to procedures, was implemented at the Haddam Neck

Plant ef fective March 31, 1986.

The new Emergency Operating Procedures (EOPs) are in final draft form,

and the first stage of classroom training has been conducted. Validation is

scheduled to be completed by the end of March,1986. Simulator training

on the EOPs will start following validation with implementation scheduled

for September,1986.

Annunciator response procedures for all applicable control room alarms

have been completed.

(D)

The Controlled Routing (CR) completion trend continues to improve. A

comparison of 1985 to 1984 indicates a 29% decrease in the backlog of CRs

even though there was a 19% increase in CRs issued. A similar trend exists

with Plant Information Reports (PIRs), which shows a 26% improvement in

the backlog of PIRs for the same time period. The data for 1986 CRs and

PIRs has not been evaluated.

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Lunctional Area: RADIOLOGICAL CONTROLS

Board Recommendatio ts:

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(A)

Efferis should be made to strengthen management oversight and

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intradepartmental communications.

An effective system for evnluating

and correcting self-identified deficiencies should be developed.

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(B)

The Ikensee should expedite efforts to seek a Techr.ical Specification

Amendment for PASS containment isolation valves to allow resumption of

full system surveillance.

UPDATE:

(A)

A task force's recommendations to improve coordination of work activities

amongst departments were presented to the Station Superintendent, and

are currently being implemented.

Many of the recommendations have

already been implemented and have been beneficial.

During refueling

outages, one individual from the operations department and one individual

from the maintenance departrnent for each shift have been assigned, as

their full time duty, to coordinate and keep abreast of the status of

equipment and work on a daily basis. Health Physics (HP) technicians now

use " zone coverage" to facilitate identifying the appropriate HP

technicians. In house HP technicians, as opposed to contractor personnel,

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are used in the field as much as possible to develop familiarity and trust

between maintenance and HP personnel.

In addition, more first line

supervision f rom HP and maintenance are active in the field.

(B)

CYAPCO submitted a proposal to revise its Technical Specifications to

allow for surveillance testing of normally closed, non-automatic

containment isolation valves that are part of the Post-Accident Sampling

System (PASS) on October 31, 1985. The proposed revision to Technical Specifications 1.8, Containment Integrity (definition) and new Table 3.11-2,

Non-automatic Containment Isolation Valves, will allow testing of normally

closed isolation valves in the PASS during operation modes 1,2,3, and 4 to

ensure opera

This revision was approved and issued by the

Commission (1pility.

as Amendment No. 72 to Facility Operating License No.

DPR-61 on February 19,1986.

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(1)

F. M. Akstulewicz, Jr. letter to J. F. Opeka, Technical Specifications to

Permit

Testing

of

the

Post-Accident

Sampling

System,

dated

February 19,1986.

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Functional Area: SUR VEILL ANCE

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Nard Recommendations:

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(A)

Continue initiatives to upgrade surveillance procedures.

(B)

Improve management control over items like CLRT issues in order to

assure that resolution is not unduly delayec.

UPDATE:

(A)

A previously existing initiative to upgrade the surveillance program is on

schedule and is expected to be completed in June,1986.

(B)

Management control over Local Leak Rate Testing (LLRT) and Integrated

Leak Rate Testing (ILRT) has been strengthened by reshapini; our

LLRT/lLRT program to achieve consistency and quhl.ity for all of NU's

operating nuclear units. Nuclear Engineering and Operations Procedure,

NEO 2.20, " Containment Leakage R. ate Testing Program," was issued on

December 10,1985.

This procedure establishes the methodology Ahd

interface responsibilities necessary to comply with 10 CFR 50 Appendix 3

requirements. Per the provisions of NEO 2.20, the Connecticut Yankee

1986 ILRT Plan was issued and is being implemented. The Plan delineates

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all NUSCO and -CYAPCO engineering responsibilities and logistical

activities necessary to conduct the ILRT.

A.s part of CYAPCO's effort to resolve containment leak rate testing concerns, a

December 23,198) submitta!(2) addressed several unresolved containment leak

rate testing issues. In addition, a comprehensive review of the status of the

Haddam Neck Plant's conformance with 10CFR50, Appendix 3 is currently being

performed and is scheduled to be submitted in March,1986.

(2)

J. F. Opeka letter to T. E, Murley, Haddam Neck - 10CFR50, Appendix 3

Compliance, dated December 23,1985.

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Functinnal Area: FIRE PROTECTION / HOUSEKEEPING

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poard Recommendations:

(A)

Maintain attention to fire barriers.

(B)

Discuss with NRC the status of findings and corrective actions related to

the Appendix R implementation program.

UPDATE:

(A)

Fire barrier integrity is , emphasized in General Employee Training, which is

given to all employees. The instrument and Controls Department held a

training session on control of fire doors and penetrations.

All of the

station fire doors that are referenced in the technical specifications have a

new sign describing in detail the commitments on fire doors.

(B)

As a result of a comprehensive (3) review of CYAPCO's position relative to

Sections ll!.G, 3, and L of 10 CFR 50, Appendix R, new exemptions and

modifications were identified.

Eight 1985(4) exemption requests were

new

subsequently filed on September 16,

which incorporated the

recommendations of the comprehensive review and the guidance provided

by Generic Letter 85-01.

The NRC Staff is presently reviewing the

exemption

requests

and

visited

the

Haddam

Neck

plant

on

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December 10,1985 to personally inspect the affected fire areas.

The non-outage related hardware modifications were completed on

August 14, 1983 in accordance with 10 CFR 50.48 schedules. Some of the

outage related work is expected to be completed during the present

refueling outage.

The need for schedular relief was identified in the

September 16,1985

submittal

for the extensive

switchgear room

modifications. Circumstances surrounding the need for relief have been

discussed informally with the Staff during the past several weeks.

A

formal schedular exemption request was submitted on March 7, 1986.(5)

(3)

W. G. Counsil letter to R. H. Vollmer, Appendix R Evaluation Status, dated

June 18,1934.

(4)

3. F. Opeka letter to H. L. Thompson, Fire Protection, dated September 16,

1985.

(5)

3. F. Opeka letter to C.1. Grimes, Fire Protection - Schedular Exemption,

dated March 7,1986.

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Functional Area: EMERGENCY PREPAREDNESS

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Board Recommendations:

(A)

Continue efforts to improve the coordination of emergency response

activities.

UPDATE:

(A)

The systematic computational comparison between licensee dose models

and those used by the state was completed on October 28, 1985. The

results of the comparison have been transmitted to the State of

Connecticut. This was the only unresolved item in this functional area.

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Functional Area: DESIGN CHANGE CONTROL /OUALITY ASSUR ANCE

Board Recommendations:

(A)

Continue implementation of DCC/CA program improvements and review

the effectiveness of the QA/OC surveillance effort.

UPDATE:

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(A)

In response to the December 13, 1984 Order modifying the Haddam Neck

license,(6) the 355 Plant Design Change Requests (PDCRs) processed at the

Haddam Neck plant from January 1,1979 through December 31,1984 were

reviewed to determine if any involved design changes of potential safety

significance. In addition,20,294 Work Permits / Orders from the same time

period were reviewed. The Plant Design Change External Review Grou

transmitted the group's final report to the NRC on September 6,1985.(p)

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included in that transmittal were the findings of the Connecticut Yankee

Plant Design Change Task Group (CYPDCTG). A plan and schedule for the

implementation of improvements in the design change process based on the

recommendations (o( the CYPDCTG were submitted to the NRC on

November 6, 1985. 81

NUSCO Quality Assurance conducted a review of the coverage and

effectiveness of quality control surveillance activities at Connecticut

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Yankee during October,1985.

The plant monitor program, designed to assess the actual "in-process

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work," was determined to need more in-field verification of ongoing

activities. Since 1984, the focus of the monitor program has been shifting

more toward operating activities of a major type such as startup testing.

The percentage of monitors involving actual in the field verification has

been steadily improving. The content of the monitor reports is currently

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being improved to provide a better description of the acti'vities observed.

(6)

3. M. Taylor letter to W. G. Counsil, Order Modifying License and Notice

of Violation and Proposed Imposition of Civil Penalty, Docket No. 50-213,

EA-84-ll5, dated December 13,1984.

(7)

D. E. Vandenburgh letter to T. E. Murley, Connecticut Yankee Plant Design

Change External Review Group Final Report, dated September 6,1985.

(8)

3. F. Opeka letter to T. E. Murley, Haddam Neck Plant Response to

December 13, 1984 Order Modifying License, dated November 6,1985.

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The QA/QC activity surveillance program, which is intended to verify that

quality controls have been established and maintained in the work areas,

needed to be reinstituted, according to the review.

More frequent

performance of activity surveillances and routine participation by QA/QC

personnel during preventive / corrective maintenance .and operational

surveillances were suggested. The use of the activity surveillance program

is being expanded by setting target goals for the number of surveillances to

be performed in particular areas. This program is being incorporated into

the tracking system for open items. Methods to improve the guidance for

performing activity surveillances are still being assessed. Periodic trend

reports are provided to management. All surveillances that result in a

quality problem result in a Nonconformance Control Report (NCR). NCRs

are trended monthly with a report to all department heads and to the Plant

Operating Review Committee (PORC).

The assessment team concluded that the development and implementation

of a strong QA/QC activity surveillance program would provide a useful

management toolin the evaluation of overall work performance.

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Functional Area: LICENSING ACTIVITIES

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Board Recommendations:

(A)

As indicated in Sections B and D, the licensee should aggressively pursue

licensing resolution in the areas of 10 CFR 50 Appendix 3 compliance and,

(B)

Operation of the post-accident sample system at power.

UPDATE:

(A)

On December 23, 1985, CYAPCO submitted a letter (9) addressing the

seven unresolved containment leak rate testing items which were identified

in inspection Report No. 50-213/84-13.(10) As part of the Haddam Neck

Plant integrated Safety Assessment Program (ISAP), CYAPCO is planning

to provide the NRC Staff with a summary of the status of compliance with

10 CFR 50 Appendix 3 by March,1986.

(B)

CYAFCO submitted a proposal to revise its Technical Specifications to

allow for surveillance testing of normally closed, non-automatic

containment isolation valves that are part of the Post-Accident Sampling

System (PASS) on October 31, 1985. The proposed revision to Technical Specifications 1.8, Containment Integrity (definition) and new Table 3.11-2,

Non-automatic Containment Isolation Valves, will allow testing of normally

closed isolation valves in the PASS during operation modes 1,2,3, and 4 to

ensure oper

This revision was approved and issued by the

Commission (abjlity.lli as Amendment No. 72 to Facility Operating License No.

DPR-61 on February 19,1986.

(9)

3. F. Opeka letter to T. E. Murley, Haddam Neck - 10CFR, Appendix 3

Compliance, dated December 23,1985.

(10)

T. T. Martin letter to W. G. Counsil, inspection Report No. 50-213/84-13,

dated October 17,1984.

(11)

F. M. Akstulewicz, Jr. letter to 3. F. Opeka, Technical Specifications to

Permit Testing

of

the

Post-Accident

Sampling

System,

dated

February 19,1986.

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Docket No. 50-20 5

BI1979

Attachment 2

Northeast Nuclear Energy Company

Millstone Unit No.1

Updated Response to SALP Report

.

March,1986

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Functional Area: RADIOLOGICAL CONTROLS

Board Recommendations:

(A)

Evaluate specific training for first-level supervisors as a measure for

improving adherence to requirements.

(B)

Upgrade adherence to routine radiation protection requirements by

individual workers.

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UPDATE:

(A) & (B)

The Nuclear Training Department acted to ensure that all station

personnel were instructed on the importance of establishment,

implementation, and maintenance of radiation protection procedures.

New Employee Indoctrination incorporates a section on Nuclear

Engineering and Operations

(NEO) Procedure familiarization,

covering the main topics of each procedure. NEO 2.05, Radiation

Protection and Maintaining Occupational Radiation Exposures As Low

As Reasonably Achievable, is included in the training.

New

employees who are potential radiation workers must take Level 1

Radiation Worker Training to receive in-depth instruction on specific

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radiological controls procedures. Instruction is given on the function,

purpose, and use of Radiation Work Permits (RWPs) and on proper

entry into and exit from radiologically controlled areas. Employees

are required to pass (80% correct) a 50 question examination, of

which 5-10 questions pertain specifically to radiological controls.

Employees are also required to demonstrate proper entry / exit

to/from

a Radiologically Controlled Area including reading

comprehension, and adherence to an RWP.

General Employee Training is given annually and includes a two hour

Level 3 Radiation Worker Requalification Program, to requalify

employees as Radiation Workers.

In the 1985 program, specific

emphasis was placed on adherence to RWP requirements, including

proper dress, documentation of radiation exposures, familiarity with

the radiological environment, and documentation of all entrances into

and exits from radiological areas.

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Functional Area: SUR VEILLANCE

Board Recommendation:

(A)

Upgrade QA of critical surveillance testing such as containment integrated

leak rate testing.

UPDATE:

(A)

Millstone Unit 1 Engineering Department Instruction 1-ENG-3.01, Primary

Containment Integrated Leak Test, was issued on June 3,1985. Detailed,

plant specific information for planning and execution of the Integrated

Leak Rate Test (ILRT), including training and inter-department

involvement, is given. The procedure is to be reviewed and revised, if

necessary, af ter receiving comments from the other NU nuclear units when

they conduct ILRTs.

Nuclear Engineering and Operations Procedure, NEO 2.20, Containment

Leakage Rate Testing Program, was issued on December 10, 1985.

1-ENG-3.01 has recently been revised and refers to NEO 2.20 in

appropriate sections. 1-ENG-3.01 is in conformance with NEO 2.20, and is

more detailed in plant specific areas.

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Functional Area: FIRE PROTECTION / HOUSEKEEPING

Board Recommendations:

(A)

Address the cluttered yard condition.

(B)

Resolve Appendix R implementation.

UPDATE:

(A)

The Radwaste Reduction Facility has been completed and was in use as of

September 27, 1985. This f acility will increase indoor storage capability.

In addition, the area near the Unit I transformer yard has been cleared of

all stored material.

(B)

As a result of a comprehensive review (1) of Millstone Unit l's position

relative to Sections Ill.G, 3, and L of 10 CFR 50, Appendix R, new

exemptions and modifications were identified.

Eight new exemption

requests were subsequently filed on November 21, 1985(2) which

incorporated the recommendations of the comprehensive review and the

guidance provided by Generic Letter 85-01. The exemption requests are

presently underg'RC review and additional information was requested by

the NRC Staff.(

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Hardware modifications which are norFoutage related are scheduled to be

completed by August 6,1986 in accordance with 10 CFR 50.48 schedwes.

Implementation of the outage related work is scheduled for the '987

ref ueling outage.

(1)

W. G. Counsil letter to R. H. Vollmer, Appendix R Evaluation Status, dated

June 18,1984.

(2)

3. F. Opeka letter to H. L. Thompson, Fire Protection, dated November 21,

1985.

(3)

Conference Call between NUSCO and the NRC Staff on January 27,1986.

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Functional Area: EMERGENCY PREPAREDNESS

Board Recommendation:

(A)

Evaluate measures f or assuring timely completion of action items.

UPDATE:

(A)

Lessons plans for emergency preparedness training have been developed

and were implemented in the 1985 emergency training. This item has been

closed out by the NRC Region 1.(4)

(4)

7. T. Martin letter to J. F. Opeka, inspection No. 50-423/85-39, dated

October 10,1985.

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Functional Area: REFUELING AND OUTAGE MANAGEMENT

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Board Recommendation:

(A)

Improve self-assessment to identify items such as f ailure to follow through

on commitments and design modifications.

UPDATE:

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(A)

Millstone Unit I commitment items have been incorporated into the Unit 1

Superintendent's assignment list, in an effort to improve tracking of

commitments.

This list has high visibility and receives significant

management attention in managing important projects on the unit. The list

is updated approximately weekly, and is distributed to all Millstone Unit I

department heads.

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Functional Area: LICENSING

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Board Recommendations:

(A)

Improve management of licensing activities to avoid late responses.

(B)

Improve coordination of activities with NRR in regard to schedule,

prioritization, and project status.

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UPDATE:

(A)

Senior NU management is routinely and aggressively involved in the

management of licensing issues. Additional resources have been added to

the licensing staff to improve the timeliness of responses. Despite the

emphasis on schedular performance, the quality of docketed submittals

cannot and will not be compromised merely to meet a deadline.

With respect to our performance in this area, we invite your attention to

comments made by the Staff at a Commission briefing on ISAP on

February 19,1986. The Staff stated to the Commission:

"So, in sum, we came up with 80 topics for Millstone Unit No. I

and 70 topics for Haddam Neck as a result of our screening

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reviewing.

Shortly thereafter Northeast began submitting the topic

reviews for Millstone Unit No.1, and between August 13th,

1985 and November 25th,1985, they submitted evaluations for

each of the 80 topics that we identified for Millstone Unit

No. 1.

I would note that that is probably the fastest response that I

have ever seen to that large a number of issues. But there

again we have to temper that judgment with the lead time that

they had from the time that we originally envisioned the

concept of ISAP. So they had done a lot of legwork. But they

pulled it together very fast."

Later in the briefing, Mr. Stello commented:

"There's one other area that we probably ought to give a lot of

credit to Northeast as a leader in how they go about doing their

analysis. They have an enormous in-house staff, and involve the

people in the plant, which has yet an additional benefit of doing

the PRA, just the way they go about it, over and above having

it done for you. And I think we ought to give them some credit

for the way they go about it, because I do think they do a very

good job."

(B)

NU's licensing group has been coordinating activities with the Integrated

Safety Assessment Program (ISAP) Project Directorate in order to

implement the program. Activities have included timely submittals of the

Millstone Unit No.1 Probabilistic Safety Study, deterministic reviews of

all Millstone Unit No.1 ISAP topics and probabilistic risk oriented project

evaluations, as well as several meetings on various aspects of the ISAP.

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Meetings on the Millstone Unit No. I Provisional to Full Term Operating

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License conversion were held with the ACRS during November and

December 1985 to facilitate NRC/ACRS approval of the license

conversion. License conversion activities are ongoing. Our view is that we

have been responsive to this recommendation, and we welcome any

additional feedback from the NRR Staff.

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Dgeket No. 50-336

B11979

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Attachment 3

Northeast Nuclear Energy Company

Millstone Unit No. 2

Updated Response to S ALP Report

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March,1986

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Functional Area: Pl. ANT OPERATIONS

Board Recommendation:

(A)

Upgrade controls over computer codes, particularly of associated

qualification certifications.

UPDATE:

(A)

Phase II of the ef fort to upgrade the control of computer sof tware used by

NUSCO for Category I engineering analysis is continuing. A Joint User

Task Force was formed to review and upgrade existing procedures on

quality related computer programs. The need for additional procedures and

controls was identified. The required procedures have been draf ted, and

are in the review process.

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Functional Area: RADIOLOGICAL CONTROLS

Board Recommendations:

(A)

Continue recent emphasis on improving radioactive material transportation

controls.

(B)

Assure better adherence to radiation protection procedures by workers.

UPDATE:

(A)

The Radioactive Materials Handling Department was reorganized to

facilitate better supervision and control of its activities.

The Health

Physics Supervisor is now responsible for the operation of this group.

A specific packaging procedure for LSA boxes, RW 6012/20612/36012,

" Packing Non-Compactible LS A Containers," was developed and ef fective

as of August 1,1985.

(B)

The Nuclear Training Department acted to ensure that all station personnel

were instructed on the importance of establishment, implementation, and

maintenance of radiation protection procedures.

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New Employee Indoctrination incorporates a section on Nuclear

Engineering and Operations (NEO) Procedure f amiliarization, covering the

main topics of each procedure.

NEO 2.05, Radiation Protection and

Maintaining Occupational Radiation Exposures As Low As Reasonably

Achievable, is included in the training. New employees who are potential

radiation workers must take Level 1 Radiation Worker Training to receive

in-depth instruction on specific radiological

controls

procedures.

Instruction is given on the function, purpose, and use of Radiation Work

Permits (RWPs) and on proper entry into and exit from radiologically

controlled areas.

Employees are required to pass (80% correct) a 50

question examination, of which 5-10 questions pertain specifically. to

radiological controls. Employees are also required to demonstrate proper

entry / exit to/from a Radiologically Controlled Area including reading

comprehension, and adherence to an RWP.

General Employee Training is given annually and includes a two hour Level

3 Radiation Worker Requalification Program, to requalify employees as

Radiation Workers. In the 1985 program, specific emphasis was placed on

adherence to RWP requirements, including proper dress, documentation of

radiation exposures, f amiliarity with the radiological environment, and

documentation of all entrances into and exits from radiological areas.

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Functional Area: FIRE PROT.ECTION/ HOUSEKEEPING

Board Recommendations:

(A)

Address the cluttered yard condition. Upgrade housekeeping in areas noted

as candidates for improvement.

(B)

Resolve Appendix R implementation.

UPDATE:

(A)

As

mentioned

in

the

Millstone

Unit

I

response

to

Fire

Protection / Housekeeping recommendations, the Radwaste Reduction

Facility has been completed. Deficiencies in other identified areas have

been corrected. The enclosure building and equipment access hatch area

have been cleaned. The area of the auxiliary building refueling water

storage tank pipe chase has been cleaned, cofferdams have been built to

prevent water f rom running down the wall, and the wall has been repainted.

The safeguards pump rooms have been cleaned and the wall in the "A" room

has been repaired.

(B)

As a result of a comprehensive (l) review of Millstone Unit 2's position

relative to Sections Ill.G, 3, and L of 10 CFR 50, Appendix R, new

exemptions and modifications were identified.

Ten new exemption

requests were subsequently drafted and are currently mdergoing internal

review. The new exemption requests are scheduled to be submitted to the

-

NRC

in April,

1986.

The exemptions have incorporated

the

recommendations of the comprehensive review and the guidance provided

by Generic Letter 85-01.

Hardware modifications which are non-outage related are planned to be

completed in accordance with 10 CFR 50.48 schedules. Implementation of

the outage related work will be scheduled following receipt of the NRC

SER.

(1)

W. G. Counsil letter to R. H. Vollmer, Appendix R Evaluation Status, dated

June 18,1984.

.,

.

[unctional Area: EMERGENCY PREPAREDNESS

'

Board Recommendation:

(A)

Evaluate measures f or assuring timely completion of action items.

UPDATE:

(A)

Lessons plans for emergency preparedness training have been developed

and were implemented in the 1985 emergency training. This item has been

closed out by the NRC Region 1.(2)

(2)

'I. T. Martin letter to J. F. Opeka, inspection No. 50-423/85-39, dated

October 10,1985.

.

.

~

.

Functional Area: LICENSING

.

Board Recommendations:

(A)

Improve management of licensing activities to avoid late responses.

(B)

Improve coordination of activities with NRR in regard to schedule,

prioritization, and project status.

UPDATE:

(A)

Senior NU management is routinely and aggressively involved in the

management of licensing issues. Additional resources have been added to

i

the licensing staf f to improve the timeliness of responses. Despite the

emphasis on schedular performance, the quality of docketed submittais

cannot and will not be compromised merely to meet a deadline.

(B)

Our perspective is that the Millstone Unit No. 2 licensing engineer and the

NRC's Project Manager for Millstone Unit No. 2 enjoy a very good working

relationship. There is virtually daily communication between the NRC and

NU in this regard with " face-to-face" update meetings at least quarterly in

order to maintain clear communications and agreements on outstanding

,

information requests and other licensing issues. Currently, the NRC and

!

NU are working together to identify items to be worked on during the next

-

year and a priority ranking for each. The mechanics are in place to ensure

that timely and responsive input is provided to the NRC.

.

.

I

!

1

I

.

l

1

,

}

.

-

,

'

Docket No. 50-336

Bf1979

.

Attachment 4

Haddam Neck Piant

Millstone Nuclear Power Station, Unit Nos. I and 2

Inputs to S ALP Evaluation Process

.

9

March,1986

a

c

,

.,

-

.

The f ollowing items provide a summary description of various meetings, letters,

,

or other transactions which we believe are relevant to the conduct of the SALP

process for our f acilities. Only a summary of each of the pertinent elements is

provided below. Further elaboration can be provided as desired.

in April,1985 in order to f acilitate an orderly transfer of a senior

o

management position, o,*r current and past Senior Vice President of

Nuclear Engineering and Operations conducted a series of meetings with

members of the Staff over a two day period.

in May,1985 we met with the Staff to discuss IGSCC inspection plans and

o

results for Millstone Unit No.1. Additionally, we kept the Staff informed

via letters and meetings, of the status of the inspection results dLring the

outage.

One of the elements of our corporate strategy regarding steam generators

o

at Millstone Unit No. 2 concerns a chemical cleaning process used during

the 1985 ref ueling outage. In May,1985 we met with the Staff to discuss

the results of this cleaning process. Additionally, information concerning

this process was made available to the indstry via available electronic

network systems and owners groups.

o

in June, 1985 we hosted a meeting with the Region ! Regional

-

Administrator, members of the Staff, and NRC consultants on the subject

of the application of PRA techniques at Northeast Utilities. Discussion

topics included technical details of our PRA techniques and the ISAP

program.

in August,1985 we entertained a one-week visit by staff personnel from

o

the 1.icense Qualification Branch, Division of Human Factors Safety and

provided information on our Production Maintenance Management System.

The resulting Site Survey Report noted that we are " committed to acting

quickly in solving problems; and to ensuring that extensive supervisory

involvement is present in every phase of each maintenance activity."

in August,1985, at the request of the Director of the Office of Inspection

o

and Enforcement (IE), we hosted a meeting with members of the IE Staff to

discuss the Pilot Outage Inspection Program. We discussed our experiences

on work recently performed for the Haddam Neck Plant which was relevant

to the formulation of the NRC Pilot Outage inspection Program,

in September,1985 we entertained a visit by the Brookhaven Reliability

o

Research Team and Mr. Carl Johnson of the NRC Division of Risk Analysis

and Operations to gather information on reliability techniques which we

have found to be effective at Millstone Unit No.1. This was in support of

NRC Technical Specification Improvement Project and Maintenance and

Surveillance Program. The resulting OSRR Project Team report noted that

,

reliability activities at NU " appear to have strong management support and

z

y

.

NU has a formalized reliability program that is conducted by a dedicated

group of individuals."

o

in September,1985 we provided comprehensive long term maintenance

records as input for the NRC Operational Safety Reliability Research

Program.

o

During 1985, as an aid in personnel transitiors within the NRC, we

,

entertained visits by the new project manager for the Haddam Neck Plant

and the new Branch Chief of Operating Reactors Branch //5 for discussion

of licensing issues concerning Millstone Unit No. I and the Haddam Neck

Plant.

o

in 1985 we were active participants in the AIF Committee on Reactor

Licensing and Safety in both the steering group concerning the source term

issue and the subcommittee on Technica! Specifications for input to the

NRC Technical Specification Task Force.

o

NU has been an active member of the Industry Effort to resolve the

USI-A-44, Station Blackout, issue. In this regard, the Industry, via the

Nuclear Utility Management and Resource Committee (NUMARC) and the

Nuclear Utility Group on Station Blackout, has been werking with the Staff

towards a mutually agreeable resolution to this issue.

o

During 1985, as chairman of the NUMARC working group on the issue of

Engineering Expertise on Shift, executive NU management continued to

work with NRC Senior Staff management and the Commission toward

development of a mutually agreeable and workable policy statement.

.

1

!