ML20149G899

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Insp Repts 50-254/97-08 & 50-265/97-08 on 970506-0616. Violations Noted.Major Areas Inspected:Operations,Maint & Surveillance,Engineering & Plant Support
ML20149G899
Person / Time
Site: Quad Cities  Constellation icon.png
Issue date: 07/11/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20149G866 List:
References
50-254-97-08, 50-254-97-8, 50-265-97-08, 50-265-97-8, NUDOCS 9707240118
Download: ML20149G899 (23)


See also: IR 05000254/1997008

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U. S. NUCLEAR REGULATORY COMMISSION

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REGION lit

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Docket Nos:

50-254, 50-265

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License Nos:

DPR-29, DPR-30

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Report No:

50-254/97008(DRP), 50-265/97008(DRP)

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Licensee:

Commonwealth Edison Company (Comed)

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Facility:

Quad Cities Nuclear Power Station, Units 1 and 2

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Location:

22710 206th ' Avenue North '

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Cordova, IL 61242

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Dates:

May 6 through June 16,1997

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inspectors:

L. Collins, Resident inspector

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K. Walton, Resident Inspector

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R. Ganser, Illinois Department of Nuclear Safety

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Approved by:

Wayne Kropp, Chief

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Reactor Projects Branch 1

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9707240118 970711

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ADOCK 05000254

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EXECUTIVE SUMMARY

Ouad Cities Nuclear Power Station, Units 1 & 2

NRC Inspection Report 50-254/97008(DRP), 50-265/97008(DRP)

This inspection included aspects of licensee operations, engineering, maintenance, and

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plant support. The report covers a 6-week period of resident inspection.

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Ooerations

Major activities such as tno Unit 2 refueling and startup were performed in a controlled

manner and essentially error free. Less significant evolutions were not always planned as

carefully and occasionally resulted in unexpected events or challenges to operatora.

Operators inappropriately used the discrete component operation process to perform

alternate system lineups for the fuel pool cooling system, drywell floor drain system, and

the feedwater system during unit shutdowns.

Maintenance and Surveillance

ihe inspectors identified, through a sampling of emergency diesel generator (EDG)

surveillance procedures, where the EDG surveillance program did not meet either the

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Technical Specification (TS) and/or the design basis documents. There was also one

example where the test methodology was not adequate to determine the sealing capability

of a check valve in the starting air system for the EDG.

Maintenance workers performed tasks safely and according to procedures. The successful

repair of the reactor core isolation cooling (RCIC) system steam supply valve was well

planned.

The inspectors reviewed and observed severallogic functional tests on Unit 2. The tests

were satisfactorily performed. The inspectors observed minor deficiencies including one

pretest brief where the test director was unprepared and a maintenance error in which a

jumper was placed in the wrong location.

Ennineerinn

The inspectors identified an inadequacy with an abnormal operating procedure for the high

pressure coolant injection (HPCI) system. TF ) procedure did not include a reference for

manually engaging the turning gear if necessary after an HPCI turbine trip.

Plant Suooort

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As low as reasonably achievable (ALARA) initiatives during the Unit 2 refuel outage helped

to reduce overall station dose to date. Radiation protection tracking and trending of dose

was improved over previous refuel outages and allowed the mid-year rev sion to the dose

goal. The 1997 station dose goal was revised from 1260 rem to 720 rem.

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The failure to take appropriate corrective action in response to identified zebra mussel

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growth in 1995 resulted in both firo pumps becoming inoperable in 1996 due to clogged

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suction strainers,

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Report Details

Summarv of Plant Status

Unit 1 entered the inspection period at full power. On May 16 a load drop was performed

to repair a leak on the RCIC system steam supply valve. Following repairs to the RCIC

valve, load was increased to full power and remained at or near full power throughout the

inspection period.

Unit 2 was shut down for refueling outage O2R14 on February 28,1997. The reactor

was restarted on June 8 and was shut down on June 10 to repair a degraded seal

condition on the 2B recirculation system rump. The unit remained shut down at the end

of the inspection period.

I. Operations

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01

Conduct of Operations

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01.1 Qbservation of Sinnificant Operations Evolutions

a.

Insoection Scone (71707)

During the period the inspectors observed major refueling outage activities for

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Unit 2. The inspectors watched reactor refueling operations from the control room

and refueling bridge, toured the drywell prior to final closcout, and observed startup

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activities including reactor criticality, power increase, and shutdown to repair the

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2B recirculation pump seal.

b.

Observations and Findinos

Refueling began May 7 in accordance with Quad Cities Fuel Handling

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Procedure 0100-01, " Master Refueling Procedure." The inspectors verified that

operators were in constant communication, recorded temperatures on an hourly

basis, and performed required checks of source range monitor (SRM) response.

Operators on the refueling bridge used three independent checks versus the

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required two when loading fuel assemblies into the reactor.

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The inspectors conducted a drywellinspection near the end of the Unit 2 refueling

outage. Drywell general material condition and housekeeping was good, notably

better than at the end of previous outages. The inspectors identified a large

amount of test wiring, previously used to transmit test data from main steam relief

valves. The licensee subsequently removed this wiring. A small amount of work

remained to be completed prior to final closeout inspections by the licensee.

During Unit 2 reactor vesselleak testing prior to startup and during startup

activities, the inspectors attended several " heightened level of awareness"

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briefings. The briefings were well coordinated and included all participating

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departments. Procedures were discussed and task responsibilities assigned. The

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inspectors observed full participation from operators and noted clear communication

with respect to potential problems, abort criteria, and expected results.

Unit 2 startup' activities were carefully conducted and essentially error free. Noted

anomalies included a single control rod drift into the core from the fully withdrawn

position and the abnormal response of the 2B recirculation pump seal pressures.

Operators promptly noted the problems and took appropriate actions. The Unit 2

reactor was subsequently shut down on June 10 to replace the recirculation pump

seal.

On several occasions operators encountered an unexpected plant response during

fairly standard evolutions. Twice a control rod drive pump tripped after starting,

and once during a teactor protection system (RPS) power supply swap for Unit 2 a '

- full reactor trip occurred. in all of these cases, plant configuration was different

than expected and operator actions resulted in an unanticipated response. The

control rod drive (CRD) pumps tripped on low suction pressure and the reactor trip

occurred because the RPS shortin0 links were installed during the power supply

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swap. Management attributed the problems to a breakdown in scheduling and

planning during the outage and took actions to ensure that all operations' activities

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were carefully reviewed prior to execution. The inspectors noted that no further

anomalies of this type occurred.

c.

Conclusions

Major activities such as refueling and startup 'ontinued to be carefully planned and

controlled. Operator performance during thex avolutions was essentially error free.

Problems with schedule control resulted in an unegected plant response on a few

occasions. No adverse consequences resulted, and corrective actions were taken

to prevent further events.

01.2 Both Standbv Gas Treatment Trains Inonerable Durino Testina

a.

Insnection Scone (71707. 93702)

The inspectors reviewed the shift engineer's logbook and spoke with operations

personnel concerning the standby gas treatment (SBGT) system inoperability,

b.

Observations and Findinas

During the performance of Guad Cities Operating Surveillance Procedure 1600 13

" Refueling Outage PCI [ Primary Containment isolation] Groups 2 and 3 Isolation

Test," on May 4,1997, operators inadvertently rendered both SBGT trains

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inoperable. On May 5 the shift engineer determined that the condition was

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reportable in accordance with 10 CFR 50.72 and initiated Problem Information Form

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(PIF) 97-2156.

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The SBGT system consisted of an A train and a B train, with the A train control

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switch normally in standby and the B train control switch in primary. The SBGT

system logic automaticaliy starts the primary train when en initiation signal is

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received, if the primary train failed, the standby train would start after a 25 second

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time delay. To test this function, the B train was taken to the off position and the

A train was placed in standby. An initiation signal was simulated, but the A train

f ailed to start after the 25 second delay.

Earlier in the test a rnaintenance error caused a fuse to blow. Test personnel

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recognized the error and proceeded to replace the blown fuse, but inadvertently

reinstalled the bad fuse. This blown fuse in the logic would have prevented the

A train from automatically starting when in standby. The error in reinstal!ing the

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bad fuse was not recognized ui.*il the test continued and the A train did not start.

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The blown fuse was replaced. During this time the operators recognized that Unit 1

was in a limiting condition for operation (LCO) in accordance with TS 3.7.P.2, but

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did not recognize that the event was reportable under 10 CFR 50.72(b)(2)(iii) as the

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occurrence of any event or condition that alone could have prevented the fulfillment

of the safety function of structures or systems that are needed to control the

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release of radioactive material. This condition existed from 8:35 p.m. to 9:15 p.m.

central standard time on May 4,1997. During this period both trains were capable

of manual start but not automatic start.

The next day the inspectors questioned the day shift engineer about the event and

required reporting and found that the shif t engineer was already reviewing the

circumstances surrounding the event. The shift engineer concluded that the event

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was reportable and an emergency notification system (ENS) call was made on

May 5,1997. Failure to report this condition within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> of discovery was a

vio!ation of 10 CFR 50.72. This licensee-identified and corrected violation is being

treated as a Non-cited Violation (50-254/265-97008-01) consistent with

Section Vill.B.I of the NRC Enforcement Policy. The inspectors reviewed the

licensee's corrective actions, which included a review of this event and reportability

requirements with licensed reactor operators.

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Conclusions

The inspectors concluded that the safety significance of this event was low since

either train could have been manually started. However, the failure to recognize a

reportable event was a concern. The licensee's corrective actions addressed the

inspectors' concern with accurately identifying reportable occurrences.

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Operations Procedures and Documentation

03.1 Use of Discrete Comoonent Ooerations

a.

Insoection Scone (71707)

The inspectors reviewed the use of discrete component operations (DCOs) and a

set of completed DCOs from April 1997. The inspectors discussed the use of

DCOs with management.

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Observations and Findinns

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Quad Cities Administrative Procedure 0230-06, " Discrete Component Operation,"

provided guidance for the operation of individual components where other

procedural guidance did not exist. A DCO was defined as a set of actions

necessary to operate a system component. The use of a DCO was not limited to

one component, since more than one component may require operation to support

the activity. The DCO process required that a request form be filled out with

appropriate action steps approved by the unit supervisor. The procedure stated

that a DCO was utilized when a component required operation for testing, such as

troubleshooting or post maintenance test verification (PMTV), or as part of a

maintenance activity such as an uncoupled pump run or, in other situations, at the

unit supervisor's discretion. The DCO was approved by two individuals, a reactor

operator or knowledgeable management person, and the unit supervisor.

The inspectors reviewed the following examples of the DCO process:

Operators used a DCO to align the Unit 2 drywell floor drain sump (DWFDS)

discharge to the floor drain collector tank rather than the normal lir.eup to

the waste collector tank, As a result of drywell activities during the cutage,

the DWFDS water was not suitable for reprocessing, and operators needed

to route the water to the floor drain collector tank. No procedure existed for

changing the lineup, and the DCO was generated on April 3,1997. This

path was used until the system was realigned to the normal configuration on

May 5,1997

Operators used a DCO during the refueling outage on Unit 2 to alter the fuel

pool cooling pump discharge valve lineup in order to throttle flow to the

reactor cavity while r0 tinuing to discharge to the fuel pool. A procedure

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existed (Quad Cities operating Procedure [QCOP] 1900-20) and could have

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been utilized with only minor changes to perform the required evolution.

Another DCO was used to control reactor water level for Unit 1 during a

shutdown when the reactor water cleanup system was not available to

reject water. This DCO directed operators to isolate leakage past the

feedwater low flow valve while the reactor water cleanup (RWCU) system

was shut down and to open the valves as necessary to add water to the

reactor vessel.

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In all three examples discussed above, operators used DCOs to perform infrequent

but necessary tasks. Each case involved an attemate system lineup and was not a

" component" operation. No adverse consequences resulted; however, the use of

D,COs rather than reviewed and approved procedures for operational activities was

a concern.

The inspectors questioned operations management about the use of DCOs. A third

party review of the use of DCOs had previously identified issues regarding potential

improper use and lack of reviaw. As a result the licensee had begun a monthly

review of DCOs and had discovered issues that were similar to the inspectors'

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findings. The licensee was aware of the examples discussed above and was

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pursuing corrective action. At the end of the inspection period, operations'

management had relayed examples of inappropr'iate use of the DCO process to all

of the operating crews and had included the appropriate rnethods for controlling the

activities (i.e., procedure field change, out of service, etc.).

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Conclusions

The inspectors found that on several occasions DCOs were used improperly. The

use of DCOs instead of reviewed and approved procedures for operational activities

could result in unexpected challenges or plant response. However, the problems

were previously identified, and the licensee had initiated corrective action.

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Operator Training and Qualification (IP 71707)

05.1 Onerator Trainina Observations

a.

Insoection Scone

The inspectors observed all or portions of the folluwing training activities:

-Two classroom sessions of initial licensed training (ILT), including the oxygen

sampling and containment emergency venting systems

Licensed operator requalification (LOR) classroom session on safe shutdown

makeup system

Two simulator sessions including " anticipated transient without scram"

(ATWS) and " recirculation pump run-up," and A post scenario critique

following the simulator session for ATWS.

b.

Observations and Findinas

The ILT class was fast paced and concentrated. The instructor was clear and

precise and closely followed the lesson plan. The inspectors noted that information

concerning containment emergency venting, in the event of a loss of coolant

accident, included clear instruction on the requirement for timely notification of

outside agencies.

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During simulator training, in one scenario, the shift technical advisor (STA) was

. located in the simulator control room at the start of the scenario. When in the

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plant, the STA is generally stationed outside the control room. The inspectors

questioned whether it would have been more realistic for the STA function to

remain outside the simulator control roorn until the scenario warranted STA

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participation. The person in the role of the STA stated that the normal practice was

for the STA to remain outside the simulator control room until required to enter by

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the simulated training event, and that this was an exception to what was the

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normal practice. The post scenario critique, following the simulator sessions, was

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interactive and constructive.

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c.

Conclusions

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In the areas observed instructors were well prepared and trainees were interactive

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in the training effort. Operations management demonstrated an active interest in

assessing and improvin0 the ;evel of training effectiveness.

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Miscellaneous Operations issues (92700)

08.1 (Closed) Licensee Event Report (LER) (50-254/93014): Intermediate Range

Monitor 11 and Average Power Range Monitor 3 Both Bypassed Without % Scram

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Being inserted. The LER stated that the cause was the f ailure to perform a self

check. The inspectors verified that all corrective actions were completed and noted

an increased use of self check and decreased number of errors since this event

occurred. This item is closed.

08.2 (Closed) Unresolved item (50-254:265/94016-03): Reactor Vessel Draining

Evolution. Quad Cities Administrative Procedure 260-3, Revision 2, " Screening for

Potential to Drain the Vessel," considered that a motor operated valve (MOV)

closcable from the control room provided sufficient isolation to prevent inadvertent-

drain down of the reactor vessel. The inspectors verified that the licensee has

since revised the procedure (Revision 5) which credits automatic isolation on low

reactor water level to prevent drain down. This item is closed.

08.3 (Closed) Violation (50-254:265/96004-01a&b): Out of Service Errors Render the %

EDG Inoperable t nd 6: ult in an Engineered Safety Features System Actuation.

The licensee couaseled individuals involved in these events and added information

to diesel generator procedures to describe the impact of removing certain fuses.

The inspectors noted a decline in out of service errors since these events occurred

in 1996. This item 6 closed.

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08.4 (Closed) Licensee Event Reoort (50-265/97009): Both Trains of SBGT Inoperable

Due to Fuse Replacement Error. See Section 01.2. This LER is closed.

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II. Maintenance

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Conduct of Maintenance

M 1.1 Surveillance Observations

a.

Insoection Scong

The inspectors observed / reviewed all or portions of the following surveillances.

OCIPM 0756-03

Local Power Range Monitor (LPRM) Calibration

QCIS 0200-28

Calibratiori ATWS High Pressure and Low Level Instruments

QCCP 0600-07

Determination of Sodium Pentaborate Concentration in

Standby Liquid Control System

OTS 0170-07

Functional Test of the Second Level Undervoltage (Bus 23-1)

~QCTS 0300-07

Functional Testing of the ATWS Recirculation Pump Trip and

Alternate Rod insertion (ARI) Logic

QCTS 0300-04

High Pressure Coolant injection Logic Functional Test

QCTS 0920-15

Strongest Control Rod Withdraw Subcritical Check

OCIS 0500-03

Instrument RPS Scram Response Time Test

OCTS 0300-07

(IP 97-0076), ATWS Recirculation Pump Test and ARI Logic

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QCTS 300-03

RCIC Logic Functional Test

OCTS 0310-03

Unit 2 Emergency Core Spray System Simulated Automatic

Actuation and Diesel Generator Auto-Start Surveillance

b.

Observations and Findinas

During a pretest brief the inspectors noted, in one case, the test director did not

appear to be fully knowledgeable of the details of the test. However, questions

generated during the brief were answered by the test director prior to commencing

with the test.

At one point during Quad Cities Technical Surveillance (OCTS) 300-03, RCIC Logic

Functional Test, the inspectors observed that test technicians were confused about

the location of a push button. Subsequently, the test was stopped until the correct

switch location was identified. The test was again stopped when a jumper was

placed on a wrong relay causing a ground condition and concurrent alarms in the

control room. Problem identification Form 97-2277 was written to address this

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problem. The licensee found that there was conflicting labeling on a relay resulting -

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from past relay swaps without subsequent removal of old labeling. The evolution

had been successfully performed in the previous fuel cycle with no known

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problems. The electrical drawing had been changed to reflect the new

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configuration, so when the test director walked down the test, he observed the

correct labeling on the correct relay. There were no panellayout drawings to show

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precise locations of relays in this panel. The test director performed a thorough

walkdown to ensure that there were no other labeling problems. Following this, the

test was successfully completed without further incident.

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The inspectors observed key portions of the emergency core cooling system (ECCS)

logic functional test, QCTS 0310-03. Operators conducted a final briefing prior to

initiation of the test. ' Contingencies were reviewed for critical steps so that

operators were certain of what action to take if the expected automatic action did

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not occu'r. Command and control was good. Each operator was given an assigned

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task and was thoroughly familiar with the actions required. The test was

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completed satisfactorily.

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C.onclusions

The inspectors reviewed and observed severallogic functional tests on Unit 2. The

tests were satisfactorily performed. The inspectors observed minor deficiencies

including one protest brief where the test director was unprepared and a

maintenance error in which a jumper was placed in the wrong location.

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M1.2 Maintenance Observations

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insoection Scone

The inspectors observed the following maintenance activities:

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Post maintenance testing of the Unit 2 reactor protection system

uninterruptible power supply,

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Overhaul of the 2A CRD pump in maintenance shop,

Licensee's activities concerning a RCIC steam valve leak,

Emergency Diesel Generator Air Start Motor Replacement,

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Modify and Install Bus 24-1 Cubicle 8 for New Breakers, and

Replace Merlin Gerin Breaker Auxiliary Switches.

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Observations and Findinos

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The inspector observed electrical maintenance technicians perform post

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maintenance testing on the Unit 2 RPS uninterruptible power supply (UPS) following

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a periodic maintenance inspection. Workers performed voltage measurements to

ensure UPS setup was in accordance with the procedure. The inspectors observed

that workers observed proper safety precautions, communicated effectively, and

carefully followed procedures.

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Work observed on the 2A CRD pump consisted of mechanical maintenance

department (MMD) personnel and a vendor representative in the process of

measuring and stacking the rotating segments of the multi stage pump onto the

shaft. This procedure required numerous trial setups. Workers carefully recorded

measurements and safely handled the sections of the pump assembly. No

discrepancies were observed in this activity.

The-Unit 1 RCIC system outboard steam supply valve, 1-1301-17, had developed a

steam leak around the seal ring. The licensee had bcen monitoring the steam leak

and, based on its progression, developed a plan to repair the valve during reduced

oower operations to limit radiation exposure to personnel. Through a good planning

effort and effective teamwork, the licensee successfully completed the repair work

with dose exposure levels below those projected.

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Conclusions

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Maintenance workers performed tasks safely and according to plant procedures.

The licensee effectively monitored the RCIC steam supply valve leakage. This

resulted in a timely and well planned repair effort. The licensee's effort to plan and

effect repairs resulted in successful repair of the valve leak with minimum dose

exposure to workers.

M3

Maintenance Procedures and Documentation

M3.1 Emeraency Diesel Generator Surveillance Procedures

a.

Insoection Scone (61726)

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The inspectors reviewed the below listed EDG surveillance procedures to determine

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if the requirements of Sections 8.3, 9.5.4, 9.5.5, and 9.5.6 of the Updated Final

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Safety Analysis Report (UFSAR) and the applicable portions of 3/4.9.A of the TS

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were properly addressed. The inspectors also reviewed the surveillance procedures

to verify that the applicable TS bases were addressed.

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OCOS 6600-01

" Diesel Generator Monthly Load Test," Revision 15

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OCOS 6600-02

" Diesel Generator Air Compressor Operability,"

Revision 9

OCOS 6600-03

" Diesel Fuel Oil Pump Monthly Operability," Revision 2

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OCOS 6600-05

" Quarterly Diesel Generator Fuel Oil Transfer Pump

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Flow Rate Test," Revision 6

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OTS 0310-06

" Emergency Diesel Generator Protective Trip Auto-Start

Bypass Surveillance," Revision 3

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Interim Procedure

"DG [ diesel generator] Trip & Alarm Switches Cal.,

97-0080

Protective Trip Bypass & Functional Test"

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The inspectors also reviewed procedure OCOS 6600-02, along with drawing M-25,

and interim Procedure 97-0080, along with drawing 4E-1350A (sheets 1 and 2), to

determine if the testing methodology described in the procedures was acceptable.

b.

Observations and Findinas

The inspectors' review of the above procedures, applicable portions of the TS, and

the UFSAR identified the following:

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QCOS 6600-01, " Diesel Generator Monthly Load Test"

Step G.1 (performance acceptance criteria) states that the generator volta 0e was

3900 to 4580 volts. The TS requirement for voltage, as stated in 4.9.A.2.c. was

4160 volts plus or minus 420 volts (3740-4580 volts). The voltage acceptance

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criteria in surveillance procedure QCOS 6600-01 was more than the TS

requirements (3900 versus 3740). Discussion with the system engir.mr

determined that the acceptance criteria was administratively controlled to

3900 volts to ensure the EDG would maintain voltage above degreded voltage

criteria in TS 3.2.B-1.6.b (3845 volts-Unit 1 and 3833 volts-Unit 2).

Section 8.3.1.8 of the UFSAR, Analysis of Station Voltages, states that the

minimum running voltage for the 4160 kV bus would be 3840 volts. The UFSAR

further states that upon an undervoltage condition where the undervoltage relays

actuate, the incoming line breakers trip, load shedding of the 4160 kV busses

initiate, and the associated EDG starts and the EDG output breaker closes when the

voltage and frequency from the EDG become satisfactory. At present the TS

requirements for EDG voltage differs from the UFSAR analysis for degraded voltage.

Even though the licensee is administratively controlling the minimum voltage during

the monthly surveillance in OCOS 6600-01, Revision 15, a TS amendment would

be necessary to establish acceptance criteria that would be in agreement with the

design basis. This issue is an Inspector Followup Item (50-254/265-97008-02)

pending submittal of a TS amendment to revise the EDG voltage acceptance criteria

to agree with the design basis.

Technical Specification basis 3/4.9, page B3/4.9-3, states that the periodic

surveillance requirements also verify that without the aid of the refill compressor,

sufficient air start capacity for each EDG is available. The basis further states that

with either pair of air receiver tanks at minimum specified pressure, there is

sufficient air in the tanks to start the EDG. Procedure OCOS 6600-01, Revision 15,

does not : quire that the air compressors be off and the air tanks at minimum

specified ptussure (230 psig). This is considered an Unresolved item

(50 254/265-97008-03) pending further discussion with the NRR technical staff.

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QCOS 6600-02, " Diesel Generator Air Compressor Operability"

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Each EDG has two banks of starting air with each bank consisting of a pair of air

receiving tanks (A'and B or C and D) and associated valves, and one starting air

compressor. One of the purposes of QCOS 6600-02, Revision 9, is to verify that

the check valves on the discharge header for each pair of air receiver tanks will

close and seal as required by the licensee's IST program. The test methodology to

verify the discharge check valve for air banks A and B will close and seal consisted

)

of the following:

1)

Isolate the C and D air receiver tanks.

2)

Close the discharge valve for the air compressor associated with banks

A and B and placing the air compressor control switch in pull-to-lock (PTL).

3)

Bleed down banks A and B to 225 to 230 psig and record the final pressure.

i

4)

Unisolate the C and D air receiver tanks.

- 5)

Af ter five minutes record the pressure for air receiver tanks A and B.

6)

Calculate the change in air receiver pressure in tank A and tank B from the

start of the test to the air pressure after five minutes, if the air pressure has

'

increased 15 psig or more, than the check valve on the discharge header for

tanks A and B had not sealed properly.

The inspectors had a concern with the above testing methodology. The air receiver

pressure would be maintained from 230 to 250 psig with the TS minimum air

pressure requirements being 230 psig. Therefore, if:

.

the air pressure in air receiver tanks C and' D during the start of the

surveillance test for the check valve for air receiver tanks A and B was the

minimum 230 psig, and

i

.the pressure in air receiver tanks A and B at the start of the test (Step 2)

was 225 psig,

the acceptance criteria'of less than 15 psig would be met even though the

discharge check valve for tanks A and B could be improperly sealed. The

inspectors consider OCOS 6600-02, Revision 9, not appropriate to ensure that the

check valves on the EDG air receiver tanks sealin the closed direction. This failure

to have an appropriate procedure is considered a Violation (50-254/265-97008-04)

of 10 CFR Part 50, Appendix B, Criterion V.

14

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4

Interim Procedure 97 0080, "DG Trip & Alarm Switches Cal., Protective Trip

'

'-

.

- Bypass & Functional Test"

The inspectors reviewed drawing 4E-1350A, sheets 1 and 2, and Interim Procedure

97-0080 to determine if the testing methodology for ensuring that the protective

-

,

high crankcase pressure trip was bypassed on auto starts of the EDG, as required

by TS (4.9.A.8.g). The inspectors determined that the testing methodology

adequately verified that all the necessary contacts required to change state for

l

bypassing the high crankcase pressure trip were tested.

c.

Conclusions

The inspectors identified, through a sampling of EDG surveillance procedures,

several examples where the EDG surveillance program did not meet either the TS

'

'and/or the design basis documents. There was also one example where the test

'

methodology was not adequate to determine the sealing capability of a check valve

.

in the starting air system for the EDG

,

M8

Miscellaneous Maintenance issues (92902)

1

-

'

M8.1 (Closed) Licensee Event Reoort (LER) 50-254/97010: "B" Control Room Ventilation

System (CRVS) Inoperable Due to Freon Leak. On April 7,1997, the licensee

identified a Freon leak from B" CRVS and declared the system inoperable. The

licensee determined the failure occurred due to vibration-induced fatigue and

'

replaced the damaged pipe. The licensee planned to assess the compressor /

i

condenser skid for vibration. The inspectors reviewed the licensee's corrective

actions and consider this LER to be closed.

Ill. Enoineerinn

E2

Engineering Support of Facilities and Equipment

E2.1

Inadeauate Hiah Pressure Coolant Iniection System Procedure

The inspectors identified a problem concerning procedure QCOA 2300-04, HPCI

Auto Trip. The high pressure coolant injection (HPCl) system control circuitry was

designed to automatically start and engage the HPCI turning gear on a coast down

following a trip of the HPCI turbine. There was a design flaw in the tuming gear

engagement mechanism whereby an engagement failure could occur in the rare

occurrence of engagement gear abutment. According to the system engineer, the

vendor has acknowledged this problem and has developed a modification to fix the

problem. The licensee has not installed this modification in the HPCI system for

either unit. The licensee developed procedure OCOA 2300-08, Tuming Gear Failure

to Start on a Coast Down, Revision 4, dated November 4,1996, to ensure

engagement of the tuming gear. The procedure for " normal" HPCI shutdown under

routine test conditions, QCOP 2300-04, HPCI System Shutdown, directs operators

to use procedure OCOA 2300-08, should the turning gear fail to engage. However,

the inspectors found that procedure QCOA 2300-04, HPCI Auto Trip, Revision 6,

15

.=

.

dated April 10,1997, did not direct the operators to enter procedure

.

OCOA 2300-08. The failure of the tuming gear to engage upon HPCI shutdown

could result in damage to the HPCI turbine, rendering it unable to perform its design

function on a subsequent initiation during accident conditions. This inadequate

procedure was another example of a violation of 10 CFR Part 50, Appendix B,

Criterion V. The licensee's raponse to this deficiency was to revise

OCOA 2300-04, HPCI Auto Trip, and reference procedure OCOA 2300-08 in the

event of a failure of the HPCI turning gear to engage following an automatic trip.

The inspectors verified that procedure Revision 7, dated May 29,1997, was

issued. The licensee did not, however, require operator training on procedure

OCOA 2300-04, Revision 7. Following the inspectors's questions about operator

training, the licensee initiated training by placing the procedure change in the

required reading binder.

The inspectors were concerned that previous problems with the HPCI turning gear

engagement, particularly on Unit 2 (LERs 25497008,26595007, and

PlF 96-1642), posed a real failure mode of HPCI upon restart when needed during

an accident situation and that the procedure used under accident circumstances did

not providc adequate instructions to cope with potential problem. Additionally, the

f ailure to provide training to operators on this potent; ally safety significant issue

~

was a weakness in the procedure revision process which did not identify the

training as required.

E2.2 Facility Adherence to the UFSAR

While performing the inspections discussed in this report, the inspectors reviewed

the applicable portions of the UFSAR that related to the areas inspected. The

inspectors reviewed plant practices, procedures and/or parameters to that described

in the UFSAR and documented the findings in this inspection report. The inspectors

reviewed the following sections of the UFSAR:

IR Section

UFSAR Section

li

A_pf cability

M3.1

8.3.1.6, 8.3.1.8

EDG,4 Kilovolt Station Voltages

E 2.1

7.8

Anticipated Transient Without

Scram

E8

Miscellaneous Engineering issues (92902)

E8.1

[ Closed) Licensee Event Reoort (50-265/95005): Automatic Scram During Electro-

hydraulic Control (EHC) System Testing. The recently installed steam line

resonance compensator (SLRC) circuit board time constant was set assuming a

standard steam line length provided by General Electric. The steam lines were

i

shorter at Quad Cities. The licensee recalibrated the SLRC, and the test was

satisfactorily performed. The same modification was performed on Unit 2 and

testing conducted in August 1996 during startup. Lessons learned from the Unit 1

transient prevented a similar event from occurring on Unit 2. This item is closed.

16

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E8.2 (Closed) Inspector Followun item (50-254:265/96004-07): Offgas Test Timor

Drawing Discrepancy. The inspectors noted that indicating lights for the timer were

not specified on the electrical schematic. The licensee confirmed that the lights

1

were originally installed in the plant but were not on the electrical drawings. A

50.59 screening concluded that no unreviewed safety question existed. The

inspectors confirmed that the drawings were updated to show the indicating lights.

This item is closed.

E8.3 (Closed) Violation 50-254:265/96017-02: Residual Heat Removal Service Water

Pump Bolt incorrect Strength, in October 1996 the licensee discovered the use of

inferior bolt materialin the 1C and 2C RHRSW pump casings while performing

maintenance on a spare RHRSW pump casing in the shop. The licensee declared

the affectbd pumps inoperable, changed the incorrect bolt material to meet design

requirements, and conducted an investigation to determine the root cause and any

other related conditions. The inspectors reviewed the licensee's immediate

corrective action and followup investigation and found them to be thorough and

adequate. This violation is closed.

E8.4 (Closed) Violation 50-254:265/96017-04: Failure to Make Required Report in

Accordance with 10 CFR 50.73. Subsequent to the licensee's discovery that the

1C and 2C RHRSW pumps were inoperable due to the use of incorrect bolt

material, between July 12,1996, and October 25,1996, Unit 2 was operated for a

period in excess of 30 days with the 2C RHRSW pump inoperable. The licensee

failed to report that Unit 2 had operated beyond the TS allowed 30-day time period

within the required reportability time. The licensee determined that the violation

resulted from failure to follow the normal process for dispositioning PIFs.

Subsequently, the licensee discussed the omission with the event screening

committee (ESC) emphasizing the importance of timely processing of PlFs and

improved tracking of open items. The licensee submitted LER 97-004 to document

the use of improper pump casing bolts and that the 2C RHRSW pump would have

performed its intended function. The inspectors reviewed the licensee's closure

activities and found them to be adequate. This violation is closed.

E8,5 (Closed) Licensee Event Reoort 50-254/97004: Residual Heat Removal Service

Water Pumps in a Degraded Condition Due to inadequate Evaluation of Replacement

Pump Casing Bolts. The licensee concluded that the affected residual heat removal

service water (RHRSW) pumps were not inoperable but degraded due to the use of

incorrect bolts in the low pressure pump casing. A bolt material having a lower

stress limit had been installed in two of the RHRSW pumps. The higher torque

value applying to the high strength material was used to install these bolts.

According to the licensee's data, the rnaximum torque limit for the installed (lower

strength) material was exceeded. However, the licensee's analysis of the removed

pump casing bolts provided conclusive evidence that bolt deformation had not

occurred and that the pumps would have performed their intended function in

accident conditions. The licensee promptly replaced the bolts in the affected

pumps upon discovery of the condition. There was also a typographical error in

section B of the LER,2nd paragraph, in which the 1C and 2C pumps were

incorrectly swapped in the text. This LER is closed.

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IV. Plant Sucoort

R1

Radiological Protection and Chemistry Controls

,

R 1,1

Revised Annual Dose Gdal

$

a.

Insnection Scone

The inspectors reviewed the licensee's data for accumulated radiation dose for the

Unit 2 refueling outage and discussed the revised 1997 annual dose estimate with

1

the station ALARA coordinator.

1

b.

_Qbservations and Findinas

~

y

The licensee revised the 1997 annual dose goal from 1260 rem to 720 rem. The

.

inspectors reviewed the licensee's data which separated the dose into five

categories - non-outage, refuel outage, contingency, emergent, and forced outage.

.

As of June 1 all five categories showed an underage when compared to the

estimate. The largest dose savings was in the area of, refuel outage. Dose savings

in the refuel outage were attributed to several factors including increased work

3

'

efficiency and good planning in the recirculation pump motor replacement and valve

work, and overall improved worker ALARA awareness. In some cases. however,

,

the dose savings was also attributed to the fact that estimates were based on

power operation of Unit 1 but the work was performed while the unit was shut

'

down, thereby reducing the dose rates in the work area.

.

4

The inspectors noted that the revision of the dose goal was based on detailed

'

tracking and trending and concluded that ALARA initiatives at the station were

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effective in reducing overall dose during the refueling outage.

'

.

}

c.

Conclusions

1

As low as reasonably achievable initiatives during the Unit 2 refuel outage helped to

,

reduce overall station dose to date. Radiation protection tracking and trending of

,

I

. dose was improved over previous refuel outages and allowed the mid-year revision

to the dose goal. The 1997 station dose goal was revised from 1260 rem to

720 rem,

.

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F8

M!scellaneous Fire Protection Issues (92904)

t

,

F8.1

(Closed) Licensee Event Reoort (50-265/93020): Continuous Fire Watch Missed for

t

the Hydrogen Seal Oil and Turbine Seal Oil Tank Deluge System. Fire protection

valves were disabled for greater than one hour and no compensatory fire watch

was established. Corrective actions included training and procedure changes. The

inspectors verified the actions were completed. This item is closed.

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F8.2 (Closed) Unresolved item (50-254:265/96011-03) and Licensee Event Reoort

50-254/96013: Zebra Mussel Fouling of Intake Structure. During the previous year

'

the licensee identified zebra mussel growth in the intake structure and documented

the condition on PIF 95-0915. The corrective actions for this PlF addressed

cleaning and repairing the intake screens, in August 1996 the licensee identified

both fire diesel pump suction strainers were fouled. Similarly, the walls of the

'

intake structure adjacent to the "B" diesel pump suction piping were about

100 percent covered with zebra mussel growth. The licensee inspected safety-

related pump suction piping and identified less than 20 percent coverage of the

interior piping. Zebra mussel growth was cleaned from component piping, strainers

and intake structure walls.

However, the licensee considered both fire pumps to be inoperable from May 6,

1996, when river water temperature increased to above 55 degrees F (the

temperature where zebra mussels are known to spawn). Both units were shut

down after May 10,1996. The inspectors considered the licensee's corrective

actions to monitor zebra mussel growth and its affects on fire pump operability to

be inadequate to detect the degraded condition of the fire protection system. The

inspectors consider this to be a Violation (50-254/265-97008-05) of 10 CFR Part 50, Appendix B, Criteria XVI, Corrective Action. This item is closed.

P8

Miscellaneous Emergency Preparedness issues

P8.1

(Closed) Licerisee Event Report 50-254/96007: Shut Down Of Unit 2 Due to High

Winds Damaging Secondary Containment. On May 10,1996, with Unit 2

operating at full power, high wind damaged secondary containment, the station

6

blackout diesel generator electrical cables, and other non-safety-related structures

and equipment. The licensee declared an alert and shut down Unit 2. Unit 1 was

already shut down for a refuel outage. The licensee repaired secondary

containment and other equipment important to operation prior to startup of the unit.

The inspectors reviewed the licensee's corrective actions and consider this item

closed.

V. Manaaement Meetinas

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management on

June 13,1997. The licensee acknowledged the findings presented.

The inspectors asked the licensee whether any materials examined during the inspection

should be considered proprietary. No proprietary information was identified.

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.

PARTIAL LIST OF PERSONS CONTACTED

Licensee

E: Kraft, Site Vice President

D. Cook, Operations Manager

. F. Famulari, SOV Director

. J. Hutchinson, Site Engineering Manager

L. Pearce,- Plant Manager

C. Peterson, Regulatory Affairs Manager

R. Svaleson, Radiation / Chemistry Superintendent

M. Waylandi Maintenance Superintendent

.

INSPECTION PROCEDURES USED

IP 61726:

Surveillance Observations

IP 71707:

Plant Operations

IP 92700:

Onsite Followup of Written Reports of Nonroutine Events at Power Reactor

Facilities

IP 92902:

Followup - Engineering

IP 92904:

Followup - Plant Support

IP 93702:

Prompt Onsite Response to Events at Operating Power Reactors

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ITEMS OPENED, CLOSED, AND DISCUSSED

,

Onened

'

50-254/265 97008-01

NCV both SBGT trains inoperable during testing

-

50-254/265-97008-02

IFl

EDG voltage acceptance criteria not in agreement with

design basis

50-254/265-97008-03

URI

TS not in agreement with procedures

50-254/265-97008-04

VIO

failure to have appropriate procedures

50-254/265 97008-05

VIO

zebra mussel fouling of intake structure

Closed

50-254/93014

LER

intermediate range monitor 11 and average power

range monitor 3 both bypassed without % scram being

inserted

50-265/93020

LER

continuous fire watch missed for the hydrogen seal oil

and turbine seal oil tank deluge system

{

50-265/95005

LER

automatic scram during EHC system testing

50-254/96013

LER

zebra mussel fouling of intake structure

50 254/96007 LER

shut down of Unit 2 due to high winds damaging

I

secondary containment

i

50-254/265-97004

LER

RHRSW pumps in a degraded condition due to

inadequate evaluation of replacement pump casing bolts

50-265/97009

LER

both trains of SBGT inoperable due to fuse replacement

eriof

l

50-254/97010

LER

"B" CRVS inoperable due to Freon leak

50-254/265-96004-01 a

VIO

out of service errors render the % EDG inoperable and

result in an engineered safety features system actuation

50-254/265-96004-01 b

VIO

out of service errors render the % EDG inoperable and

result in an engineered safety features system actuation

50-254/265-96017-02

VIO

RHRSW. pump bolt incorrect strength

50-254/265-96017-04

VIO

failure to make required report in accordance with 10 CFR 50.73

'!

-265-94016-03

URI

reactor vessel draining evolution

50-254/265-96011-03

URI

zebra mussel fouling of intake structure

50-254/265-96004-07

IFl

offgas test timer drawing discrepancy

Discussed

None

21

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LIST OF ACRONYMS USED

ALARA

As Low As Reasonably Achievable

r

ARI

Alternate Rod insertion

JATWS -

Anticipated Transient Without Scram

,

'CFR

Code of Federal Regulations

Comed

Commonwealth Edison Company

CRD

Control Rod Drive

~CRVS

' Control Room Ventilation System

DCO-

- Discrete Component Operations

DG

Diesel Generator

DWFDS

Drywell Floor Drain. Sump

ECCS

Emergency Core Cooling System

EDG

Emergency Diesel Generator

i

EHC

Electro-Hydraulic Control

ENS

Emergency Notification System

ESC

J

HPCl ^

Event Screening Committee

High Pressure Coolant injection System

~

IDNS

Illinois Department of Nuclear Safety

j

IFI'

Inspector Followup Item

i

ILT

Initial Licensed Training

IM

Instrument Maintenance

-

IST

inservice Test

kV

Kilovolt

LCO

Limiting Condition for Operation

LER

Licensee Event Report

LOR.

Licensed Operator Requalification

'

LPRM

Local Power Range Monitor

MMD'

Mechanical Maintenance Department

MOV

Motor Operated Valve

NSO-

Nuclear Station Operator

PCI

Primary Containment isolation

PDR

Public Document Room

PlF

- Problem Identification Form

PMTV

Post Maintenance Test Verification

PTL

Pull-to Lock

QCCP

Ouad Cities Chemistry Prucedure

OCIPM

Quad Cities instrumern Prevent Maintenance

OCIS

Quad Cities Instrument Surveillance

OCOA

Quad Cities Abnormal Operating Procedure

OCOP

= Quad Cities Operating Procedure

OCOS

Quad Cities Operating Surveillance Procedure

OCTS

Quad Cities Technical Surveillance

OTS

Quad Cities Technical Surveillance

RCIC

Reactor Core Isolation Cooling

RHRSW

Residual Heat Removal Service Water

RPS

Reactor Protection System

RWCU

Reactor Water Cleanup

22

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'a

SBGT

Standby Gas Treatmer.t

SLRC

Steam Line Resonance Compensator

SRM

Source Range Monitor

}

STA

Shift Technical Advisor

TS

Technical Specification

-

UFSAR

Updated Final Safety Analysis Report

UPS

Uninterruptible Power Supply

,

URI

Unresolved item

VIO

Violation

WR

Work Request

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