ML20141F859

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Submits TMI-2 Cleanup Weekly Status Repts for 851223-29 & 30-860105
ML20141F859
Person / Time
Site: Crane Constellation icon.png
Issue date: 01/06/1986
From: Travers W
Office of Nuclear Reactor Regulation
To: Harold Denton, Miraglia F
Office of Nuclear Reactor Regulation
References
CON-NRC-TMI-86-003, CON-NRC-TMI-86-3 NUDOCS 8601090571
Download: ML20141F859 (4)


Text

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cc - y c January 6,1986 NRC/THI-86-003 MEHORANDUM FOR:

ihrold R. Denton, Director Office of Nuclear Reactor Regulation Frank J. Niraglia, Director Division of PUR Licensing-B FROM:

William D. Travers, Director THI-2 Cleanup Project Directorate SU3 JECT:

NRC THI-2 CLEANUP PROJECT DIRECTORATE WEEKLY STATUS REPORT FOR DECE!!BER 23, 1985 - DECEMBER 79, 1985 AND DECEMBER 30, 1985 - JANUARY 5, 1986 1.

DEFUELING The licensee completed loading one side loading debris bucket with pieces cf fuel rods. The bucket containing about 30 lbs. of debris was placed in a fuel canister. Currently two defueling canisters are fully loaded and two are partially loaded.

The licensee completed the installation and testing of the debris vacuum system during the week of December 23, 1985. The system uses an air driven submerged pump to pick up a slurry of fuel debris and water. Debris ranging from about 140 microns up to fuel pellet size are collected in a knockout canister and smaller particles ranging in size down to 0.5 microns are removed from the effluent fluid stream by filter canisters. The knockout and filter canisters serve as the storage and shipping containers for the debris.

The licensee began vacuun defueMng on December 31, 1985. About 300 lbs. of debris has been loaded into the knockout canister which has a capacity of about 1,800 lbs. The licensee is working to improve the debris pick up rate of 1 to 2 lbs. per minute that has been achieved so far.

2.

PLANT STATUS The facility remains in long tem cold shutdown with the Reactor Coolant System (RCS) vented to the reactor building atmosphere and the reactor vessel head and plenum assembly removed from the reactor vessel.

The plenuta is on its storage stand in the deep end of the fuel transfer canal. A dan has been installed between the deep and shallow ends of the fuel transfer canal. Tha deep end is filled with water to a depth of about 20 feet (about 5 feet above the top o f--the-plenum)

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Janaury 6,1936 Frank J. Miraglia NRC/Ti41-36-002 The modified internals indexing fixture is installed on the reactor vessel flange and is flooded to elevation 327 feet 6 inches (151 feet above the top of the core region). The defueling platform is installed over the internals indexing fixture.

Calculated reactor decay heat is less than 12 kilowatts.

RCS cooling is by natural heat loss to the reactor building ambient a trusphere.

Incore themocouple readings range fron 68'F to 95 F with an average of 82 F.

The average reactor building temperature is 50*F.

The reactor building airborne activity at the Westinghouse platform is 1.1 E-8 uCi/cc Tritium and 1.6 E-10 uCi/cc particulate, predominantly Cesium 137.

Spent Fuel Pool "A" is flooded to a depth of 20 feet. About 6 feet of water is over the fuel canister storage racks.

3.

UASTE t'ANAGEMENT EPICOR II completed processing Batch 271 which consisted of recirculation of water froa CC-T-2 for particulate removal. The total processing volume was about 60,000 gallons. Batch 272 and 273 were completed for a total of about 15,000 gallons from the Submerged Demineralizer System (SDS) monitor tanks.

SDS is temporarily shutdown.

Total volume processed through SDS to date is 3,598,397 gallons, and the total volume processed through EPICOR II is 2,776,536 gallons.

4.

DOSE REDUCTION /DECONTA'lINATION ACTIVITIES Decontamination activities are continuing on the 281' level of the auxiliary building. Kelly-vac cleaning of the decay heat vaults is in progress.

Average general area radiation dose rate is 40 mren per hour on the 347' level of the reactor building and is 67 mrem per hour on the 305' level of the reactor building.

Decontamination of the "A" D-ring is complete.

5.

ENVIRONMENTAL HONITORING US Environmental Protection Agency (EPA) sample analysis results show THI site liquid effluents to be in accordance with regulatory limits, NRC requirements, and the City of Lancaster Agreement.

THI water samples taken by EPA at the plant discha.9e to the river consisted of seven daily composite samples taken from December 8 through December 14, 1985 and from December 15 through December 21, 1985. A gama scan detected no reactor related activity.

The Lancaster water sample taken at the water works intake and analyzed by EPA consisted of a s a en day composited sample taken fron December 8 through December 14, 1985 and from December 15 through December 21, 1985. A gamma scan detected no reactor related radioactivity.

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Janaury 6, 1986 Frank J. iliraglia fiRC/Tt!!-86-002 The flRC outdoor airborne particulate sai 2r at tne Till site collected a sample between December 18 e J Decenber 26, 1985 and between December 26, 1985 and January 2, 1936. fia reactor related radioactivity was detected. Analysis showed ludine-131 and Cesium-137 concentrations to be less than the lower limits of detectability.

6.

REACTOR RUILDIllG ACTIVITIES Initial vacuum defueling of the reactor core is in progress.

The pressurizer manway cover hu been removed and the access part shielded. Sludge samples have been 'emoved from the pressurizer aied further examination is in progress.

7.

AUXILIARY AfiD FUEL !!ANDLING BUILDit!G ACTIVITIES Installation of the balance of DUCS cuntinued.

Spent Fuel Poal "A" has been flooded to a depth of about 20 feet

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l 8.

fiRC EVALUATIONS IN PROGRESS Techaical Specification Change Request number 49.

Recovery Operations Plan Change number 31.

SDS Technical Evaluation and System Description Update.

Core Stratification Sample Safety Evaluation.

Defueling Water Cleanup System Technical Evaluation Report, Revision 7.

Containnent Air Control Envelope Technical Evaluation Report, i

Revision 5.

Solid Waste Facility Technical Evaluation Report.

9.

PUBLIC fiEETIfi.G_S.

The next neeting of the Advisory Panel is scheduled for February 12, 1986 at the Holiday Inn, 23 South Seccnd Street, liarrisburg, PA from 7:00 PM to 10:00 Plt.

Persons desiring the opportunity to speak before the panel are asked to contact fir. Thamas Smithgall at 717-291-1042 or write to him at 2122 tiarietta Avenue, Lancaster, Pennsylvania 17603.

DMGMMUNuc Efi William D. Traverg Hilliam D. Travers Director THI-2 Cleanup Project Directorate

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Janaury 6, 1986 Frank J. fliraglia NRC/TMI-86-002 INTERNAL DISTRIBUTION E00 OGC Office Directors Commissioner's Technical Assistants NRR Division Directors NRR A/D's Regional Administrators IE Division Directors TAS EIS THI Cleanup Project Directorate (10)

PHS EPA DOE RI Division Directors Public Affairs, RI State Liaison, RI TMIPO iiQ r/f THI SITE r/f CENTR 1L FILE iiRC PDR LOCAL PDR TMI-2 Project Section File m

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