ML20086L185

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Telecopy AO 74-21:on 740411,pressure Switch PS-2-5-14C & PS-2-5-14D Found Inoperable.Caused by Blockage in Sensing Line.Setpoint Adjusted & Leads Lifted to Provide Proper Inputs to RPS Logic
ML20086L185
Person / Time
Site: Peach Bottom Constellation icon.png
Issue date: 04/12/1974
From: Ullrich W
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20086L190 List:
References
AO-74-21, NUDOCS 8402070453
Download: ML20086L185 (1)


Text

PcIch Bottoa Ato c wer o a on jdh 3.$ R. $ /( d 1 5 4f~337'//Chy'i'l 6

Delta, Pennsylvania b

April 12, 1974 Ul i

Mr. James P. O'Reilly, Director l

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United States Atc=ic Energy Co-aission

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Directorate of Regulatory Operation,

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1 631 Park Avenue j

King of Pruccia, Pennsylvania 19406 i

a Bubject:

Abnor-al Occurrence 24-Hour Notification j

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Confirming r.y conversation with Mr. R. A. Feil, A.E.C. Region I Rt6ulatory Operations Office on April 12, 1974 1

Reference:

License Nu=ber UFR 44, Anendment Number 1 i

Technical Specification

Reference:

Note 4 to Table 3 1.1 l

Report No.:

50-277-74-21 Report Date:

'nril 12,1974 i

Occurrence Date:

April 1.1, 1974 L

Facility:

Peach Botton Atomic Power Station R. D.1 Lolta Ibnnsylvania 17314 Identifict. ion of Occurrence:

Inoperability of PS-2-5-14C and PS-2 + 14D Conditions Prior to Occurrence:

Plant at 2% Power Description of Occurrence:

During the pinnt start-; a to greater than 30% power, the operability of the preccare ewitchen which cence turbine first stage pressare were tonitored.

It was rated that all the prermure evitches failed to operate at the 30%

power level. Before proceeding up in power above 30%, the setpointo on the e

cwitchee were adjunted to provide the proper logic input to the RPS aystem.

During the subsequent chutdown, these pressure cwitches were recalibrated

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in accordance with a new curve of first stage turbine pressure vercus power based on data obtained during the previous operation. Duving the next start-up, the C and D pressure evitches failed to operate at the correct turbine power level and were again readjunted to provide proper logic input S$

before exceeding 30% power.

Subsequent investigation determined that the s

@7 sensins line from the turbine was not delivering the proper preocure signal 1

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$8 to th-ce two evitches. Because. plant conditions prevented access to portions n

bg of the sensing line, the wires to the proper ' logic relays were lifted to'~

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provide the proper EPS logic inputs.

4 Designation of Apparent Cause of Occurrence-1 3@

It is presently believed that a blockage exists in the semaing line frem d

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= g.._lhtfirst.cMat Drbine ptercure toJTe-2-5-14 and_D._Thie. blocaze my_bt__ _...__ W a closed root valve. 'ihio valve is inaccesetble at the present time.

og to o.tn Acalysis of 0;currence:

There are to cafety implications aceociated with this occurrence because the

. inputs to'the. Pld uycten were alvajaTn the safe direction., Supervicory j

personne1 ensureo proper position at the turbine trip scram bypass relays r--

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Corrective Action:

On each occassion.vb-proper relay operation did no cur, setpoint '

adjusteents were ca

. r 1cado were lifted to provid-4 roper inputo to the RPS logic. These action; woro conservative in that they ensure a reactor ceras fron turbine trip at any power level (not only above l

30% power). Final corrective action cuot 'avait the next plant shutdown.

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Failure Dato'

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. None.

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Very,truly yours, i~

y pfQ V. 7. Ullrich, Superintendent s

Peach Bottos Atomic Power Station.

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