ML20086L176

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Telecopy AO 74-22:on 740416,HPCI Tripped During Reactor Vessel Injection Test.Caused by Greater Acceleration Rate During Start.Hpci Controls Checked.Sys Operability Test Will Be Performed
ML20086L176
Person / Time
Site: Peach Bottom Constellation icon.png
Issue date: 04/17/1974
From: Ullrich W
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20086L173 List:
References
AO-74-22, NUDOCS 8402070449
Download: ML20086L176 (2)


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April 17, 1974 O

i Xr. James P. O'Reilly, Director

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United States Atc=ic Energy Cc=ission Directorate of Regulatory Operations g3 7 /g 631 Park Av.nue King of Prussia, Pennsylvania 19406

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l Subiect :

Abner al Occurrence 2h. Hour Notification Confir=ing cy conversation with Mr. Ed Greenman, A.E.C. Region I Regulatory Operations Cffice on April 17. 1974

Reference:

1,1 cense Nunber DPR 44. Amend =ent Nu=ber 1 Technical Specification 3 5.C.1 Report No.:

50-277-74-22 Report Date:

April 17, 1974 Occurrence Date: April 16. 1974 Facility:

Peach Bottos Ato:ie Pcwer Station, R.D.1, Delta, Pennsylvania 17314

  • Identification of Occurrence:

HPCI tripped during renctor vessel injection test.

Conditiens Prior to Occurrence:

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. Plant shutdown following a p1nnned turbine trip and ocram fro: M power.

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Designation of Occurrence:

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As part of the start-up test progr., an HPCI system test which delivers

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water to the reactor vessel is required. This test was performed on 1

4 April 16, 1974 following a planned turbine trip and reactor scram from the 50% power level.. Upon auto..atic initiation, the EMI turbine isolated.

Icolation was caused by a high steam flow ccndition to the turbine. High I

stea= flow was sensed bv a differential pressure switch connected to an elbow tap flow ele ent in the steam cupply to the HPCI turbine. The isolation was i=ediately reset by the operntor. This per=itted the HPCI to restart and cuccessfully, injected water to the reactor vescel at rated flow. Data taken during this test indicated additional control adjuste=ents are require 3.

g Desi mation of Apparent Cause of Occurrence:

Data tt%en during the EPCI injettic: test shows that turbine acceleration rate during the initial start was significantly g-eater than during the restart. Thie infers that the stea= flow during the initial sta-t was also significantly greater than bring the restart. The precise cauce has not been deter =ined at this time.

Analyeis of Occurrence:

The initial isolation of the HPCI system during the infection test has no '

p safety i=plicatiene in that the system was de=cnstrated i=:ediately to gf q be capable of injecting water to the reactor vessel.

Start-up tecting q

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is perfor=ed for the purpose of identifying and correcting ninor control proble=s with engineered cafegusrd systems prior to achieving reactor 18 power levels where design system response it, required to citigate accidents. O B402070449 740426 PDR ADOCK 05000277

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Corrective Action:

1 Folleving this coeurrence, the EPCI controls were checked. No l

ccnditiens.hi:h would account for the initial high flow g

were identified.

System operability testa chall be perforced during the next start-up at apprcxirstely 400 pcig reactor preerure.

System automatic initiation tests shall be perfor:ed at rated reactor pressure ucing the pu=p test loop flev path.

Vessel injection testa shall be repeated at a nominal 514 power level-Failure Octa:

No previcus ci=ilar EPCI failures have been experienced.

Of' W. T. Ullrich, Superintendent Fench Botto: Atenie Power Station.

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