ML20038C736

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IE Insp Repts 50-317/81-22 & 50-318/81-21 on 811022-30. Noncompliance Noted:Failure to Change Containment Isolation Valve Failure Mode for Over 5 Yrs & Use of Wrong Valve Failure Mode
ML20038C736
Person / Time
Site: Calvert Cliffs  Constellation icon.png
Issue date: 11/25/1981
From: Architzel R, Mccabe E, Rhoads G
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20038C723 List:
References
50-317-81-22, 50-318-81-21, NUDOCS 8112140086
Download: ML20038C736 (5)


See also: IR 05000317/1981022

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U.S. NUCLEAR REGULATORY COMMISSION

OFFICE OF INSPECTION AND ENFORCEMENT

REGION I

50-317/81-22

Report No.

50-318/81-21

50-317

Docket No.

50-318

DPR-53

C

License No.

DPR-69

Prierity

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Category

C

Licensee:

Baltimore Gas and Electric Company

P.O. Box 1475

Baltimore, Maryland 21203

Facility Name: Calvert Cliffs Nuclear Power Plant, Units 1 ar.d 2

Inspection at: Lusby, Maryland

Inspection conducted: October 22 - October 30, 1981

Inspectors:

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G. G. Rhoads, FIeactor Inspector

date signed

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R. E. Architzel, S,enior Resident Inspector

date signed

Approved by:

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E. C. McCabe, Jr. , Cnief, Reactor Projects

date signed

Section 28, DRPI

Inspection Su mary:

Inspection on October 22 - October 30, 1931 (Combined Report Nos. 50-317/S1-22

and 50-318/81-21)

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Areas Inspected:

Routine, onsite inspection of valve failure mode by a Region

I inspector and by the resident inspector.

Three violations were identified:

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Failure to change containment isolation valve failure mode for over 5 years;

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Failure to take measures to preclude recurrence of improper valve f ailure

mode; Electrical schematics showed wrong containment isolation valve f ailure

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mode.

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86 812197

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OETAILS

1.

Persons Contacted

The following technical and supervisory level personnel were contacted:

  • J.

T. Carroll, General Supervisor, Operations

  • W.

C. Gibson, General Supervisor, Electrical and Controls

'O. W. Latham, Principal Engineer, Operational, Licensing and Safety

Unit

P. G. Rizzo, Assistant General Foreman, Maintenance

  • L.

B. Russell, Plant Superintendent

J. Sites, Supervisor, Instrument Maintenance Unit 1

J. A. Snyder, Supervisor, Instrument Maintenance Unit 2

  • J. A. Tiernan, Manager, Nuclear Power Department

W. L. Whitaker, Assistant General Foreman, PMD

  • Attended exit on Octob9r 30, 1931.

Other licensee employees were also contacted.

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2.

Review of Events Requiring One Hour Notification to the NRC

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On October 22, 1931 at 3:30 p.m. the licensee declared the Unit One

air-operated Component Cooling Water supply valve to containment

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(1-CC-3832-CV) inoperable after realizing it would fail OPEN on loss of

instrument air.

The licensee reported this to the NRC Emergency

Operations Center at 4:25 p.m., and began a reactor shutdown.

The valve

was declared operable at 8 p.m. after the licensee had modified the

actuator to cause the valve to f ail SHUT on loss of air.

About 10:30

p.m.,

October 22, 1981 the inspector reviewed the following:

FSAR Table 5-2, Sheet 2 of 4; FSAR Figure 7-10, Sheet 2; FSAR Figure 9-6;

FSAR Figure 9-25.

No difference was found between Unit 1 (Valve 1-CC-3832-CV) and Unit 2

(Valve 2-CC-3821-CV).

The inspector then examined the Unit 2 solenoid

for Valve 2-CC-3332-CV and noted it appeared to be deenergized with the

valve OPEN.

Ha asked the Shift Supervisor about that.

The Supervisor

stated that Instrument and Control Technicians had examined the Unit Two

valve and determined that it would fail SHUT on loss of air or of

electrical poner to the solenoid.

The inspector told the General

Supervisor, Operations about his examination of the solenoids and

schematics, and about his conclusion that the Unit Two valve would fail

OPEN on loss of air and electrical power.

About 2:50

a.m., October 23, 1981, after further review, the licensee

declared t',e Valve 2-CC-3832-CV inoperable after determining it failed

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OPEN on loss of air or electrical power.

This was reported to the NRC

Emergency Operations Center at 3:40 a.m.

The valve actuator was modified

to fail the valve SHUT on loss of air or electrical power; Valve

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2-CC-3832-CV was declared operable at 9:30 a.m.

The inspector witnessed

parts of the post-maintenance testing and found no discrepancies.

On October 27, 1981 the inspector reviewed MR's (Maintenance Requests)

MSl-432 for the work performed on the Unit One valve, and IM-81-2127 for

the work performed on the Unit Two valve.

Both MR's referenced Field

Change Request FCR 75-1089, Revision Two, originated September 2, 1976.

It stated that it revised FSAR Table 5-2 to show the valve as

fail-closed, revise FSAR Figure 5-10, and changed the pneumatic failure

mode of the valve. The stated reason was that failing closed was the

conservative failure mode and would provide additional isolation

capability. The FCR work description states that the FCR made

1-CC-3832-CV fail closed on loss of air and on loss of electrical power.

FCR 75-1089, Revision 2, was not approved by the Plant Operating Safety

Review Committee until October 22, 1981, over five years from the time it

was initiated.

10 CFR 50 Appendix B Criterion XVI requires measures for

promptly correcting conditions adverse to quality.

Failure to process

FCR 1089 for more than five years violates that requirement.

(317/81-22-01)

The inspector questioned the General Supervisor, Operations, on how Valve

1-CC-3832-CV had been determined to be inoperable.

The Supervisor stated

that, while investigating a problem with ASCO solenoid valves, the

licensee had determined that the Unit One CCW supply valve to containment

would fail OPEN.

Upon further investigation, the licensee determined

that CCW inside containment was not considered safety-related, and was

therefore not seismically qualified.

Instrument air to the valve

actuator was also not seismically qualified.

Consequently, a seismic

event could cause a CCW line break inside containment and also cause CCW

Containment Supply Valve 1-CC-3832-CV to fail 0 PEN. CCW could then empty

into containment; its safety-related functions would be lost.

CCW

outside containment supplies water to the low and high pressure coolant

injection seals and cooling water to the shutdown cooling heat exchangers

(which cool Containment Spray).

The inspector verified that the "Q" drawing for Unit One CCW showed that

the boundary for the safety-related portion of the CCW system did not

include piping inside containment.

On October 27, 1981 the Principal Engineer, Electrical Engineering

Department, stated that CCW since containment t.as a "two over one"

system, meaning that it should not fail and damage any+.hing seismic. The

inspector asked if the piping was supported so that it would not break

during a seismic event. The Principal Engineer stated that this was not

the intent of the "two over one" concept, but rather that the pipe would

be restrained so that it could not affect seismically qualified systems.

On October 30, 1981 the licensee showed the inspector a March 13, 1974

letter (serial CC-5639) from Bechtel Power Corporation to the Project

Engineer of Baltimore Gas and Electric Company.

The letter stated that

Bechtel had performed a seismic analysis on the CCW system and it could

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be considered seismically qualified. The licensee' stated they planned to

review all CCW maintenance since March 1974 to show whether the seismic

capability had been altered. That data will be reviewed when available.

On October 27, 1981 the inspector asked the General Supervisor,

Electrical and Controls, why the Unit Two valve had not been determined

to be inoperable before the inspector discovered the deenergized

solenoid. The Supervisor stated that the technicians had verified that

the air supply and vents were connected to the solenoid valve the same

way as in Unit One but did not verify the electrical hookup.

The

Supervisor also stated that no electrical work had to be performed on

Unit One's solenoid valve since it would~have failed SHUT on loss of

electrical power.

On October 28, 1981 the inspector reviewed controlled electrical

schematic lE-76, Sheet 14G, Revision 1, February 16, 1977.

It showed

that the solencia valve ICV-3832 was electrically connected to fail OPEN

on loss of electrical power. The inspector next reviewed documentation

of work performed on valve 1-CC-3832-CV since 1972. On July 24, 1973 a

control valve and actuation information sheet had been filled out

indicating the valve would fail OPEN on loss of air, but did not indicate

how it would fail on loss of electrical power.

No other work was

documented for the valve's electrical power. A controlled drawing,

(IE-76, Sheet 14G, Revision 1, February 16,1977) indicated the valve

should be electrically connected to fail OPEN on loss of electrical

power, but the licensee had found the valve to be connected electrically

to fail SHUT on loss of electrical power.

10 CFR 50 Appendix B Criterion

IV requires appropriate drawings for activities affecting quality. This

violates that requirement (317/81-22-02).

On October 29, 1981 the inspector asked the Assistant General Foreman,

Maintenance, and the Principal Engineer, Operational Licensing and Safety

Unit, why FCR 1089, had taken so long.

The Principal Engineer stated

that the FCR may have been misfiled at the plant because it first

discusses an FSAR table (Table 5-2) which needed updating.

The Principal

Engineer theorized that the FCR was then given a low priority for

completion due to the FSAR needing updating only.

The Assistant General

Foreman, Maintenance showed the inspector a Responsible Engineer February

1981 Field Change Request computer list which indicated that construction

was complete for FCR 1089, Revision 2 and on October 1,1981 Facility

Change Request Data Base which showed FCR 1089, Revision 2. He stated the

Responsible Engineer computer list was apparently in error, but he had

not been able to track down when the error had been made.

In addition to requiring measures for prompt correction of conditions

adverse to quality, 10 CFR 50 Appendix B Criterion XVI requires that

corrective measures be taken to preclude recurrence.

Since the licensee

corrective measures did not address the sa.ne problem on Unit 2, the

measures to prevent recurrence were not adequate and violate NRC

requirements. (317/81-22-03; 318/81-21-01)

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3.

Review of Licensee Event Reports (LER's)

The inspector reviewed LER's submitted to NRC:RI to verify that the

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details of the event were clearly reported, including the accuracy of the

description of cause and adequacy of corrective action. The inspector

determined whether further information was required from the licensee,

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whether generic implications were indicated, and whether the event

warranted onsite followup.

The following LER's were reviewed.

LER No

Date of Event

Date of Report

Subject

81-74

October 22, 1981

October 23, 1981

Inoperability

(Unit One)

of

Component

Cooling

Isolation

Valve.

81-45

October 23, 1981

October 23, 1981

Inoperability

(unit Two)

of Component

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Cooling

Isolation

Valve.

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For both LER's, the inspector verified that appropriate corrective action

was taken or responsibility assigned and that continued operation of the

facility was conducted in accordance with Technical Specifications and

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did not constitute an unreviewed safety question as defined in 10 CFR 50.59.

Report accuracy, compliance with current reporting requirements,

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and applicability to other site systems and components were also

reviewed.

See Paragraph 2 for further details.

4.

Exit Interview

Meetings were held with senior facility management on October 30, 1981

to discuss the inspection scope and findings.

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