LER-1980-001, /03L-0:800102,while Operating at Approx 98% Power, Breaker Feeding Containment Cooling Fan Motor VA-3B Tripped.Caused by Trip Units Out of Calibr.Units A&C Were Replaced,Calibr & Tested Satisfactorily |
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EVENT DESCRIPTION ANO PROBA8LE CONSEQUENCES h o
2 l On. January 2, 1980, while operstinz st sperexiestely C never, the brener faedi w I o ia lthe containment cooling fan =otor (7A-33) tripped.
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l occurred due to faulty trip units in the bresker f*eeding 7A-33.
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- iC7 h03P vas repaired by sd-I 3
[ justing / cleaning an orifice in the vslve controller which had been plurged.
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0=sha Public Power District Fort Calhoun Station Unit Ho. 1 Decket No. 05000235 IIR SC-001 Attach =ent No. 1 Safety Analrsis The Contain=ent Air Recirculation, Cooling and Filtering System at the Fort Calhoun Station Unit No.1 is so designed that no single failure can prevent the syste= frc= performing its designed function.
During this incident, the contain=ent cooling and filtering unit 7A-33 was rendered inoperable as a result of a faulty feeder breaker.
In addition, during subsequent operability testing of redundant contain=ent ecoling and filtering units, ECV h033 was found to be inoperable iue to a plugged orifice in the pneu=atic controller which feeds air to/frc= the valve's diaphram.
ECV h033 is the c =penent cooling water inlet valve which feeds the coeling coil for the con-tai--ar* ~^oling fan, 7A-73.
Fol10ving the failure of HCV 4033, diesel D1 was tested and verified operable and the Contain=ent Spray System, which is inde-pendent of and redundant to the Contain=ent Air Recirculation and Ccoling Syste=, was also fully operable during the incident.
This contain=ent spray 37ste= is designed for s tinimum heat re=cval capacity of 260 x 10~ 3TU/hr. vith a containment temperature of 233 F; this is the heat re=cval rate necessary to maintain the conta1=nent at=osphere below the designed pressure in ne even* af a 03A.
The 230 x 10 3TU/hr. heat rencval rate ccrresponds to a containment spray flow rate of 3L00 gp=.
This 3h00 sp= correspends to the case of =ini=u= flow rate - that is, three spray pu=ps starting and only one spray header available.
It is a point of interest to note that with two contain=ent spray pu=ps available and two spray headers - the contain=ent spray system is capable of supplying a flow rate of $100 gp=.
Thus, it is dee=ed that the Fort Calhoun Contain-
=ent Spray Syste= is, by itself, = ore than capable of supplying sufficient contain=ent cooling in the unlikely event of a 03A.
1944 542 At the time of the incident, 7A-33 was considered inoperable due to a faulty breaker and 7A-7D vas also considered inoperable since HCV h033 (the 00=ponent cooling water inlet valve) was not functioning as designed. However, the remaining and operable centain=ent eccling and filtering units 7A-?A and 7A-7C vere still capable of re=0Ving 210 x 10 3TU/hr. at DBA conditions, frc= the contain=ent at=csphere.
Thgsis755oftherequiredcontain=ent03Aheatre=cvalrateof280x 10 3TU/hr.
7A-7D vaa rendered inoperable as a result of the HC7 a033 c:=penent cooling vater valve failure.
However, the rav vater syste:
'g was operable and is a backup supply for cc=ponent c0 cling vater to the
.s 7A-73 cooling coil.
Thus, as far as the safety inalysis is conecrned, N-7A-70 could have been =anipulated to supply centainment c00 ling as de-m signed and the 03A heat re= oval rate of 250 x 10' 3TU/hr. could have been
=e by the COntain=ent Cooling and Recirculating fan units if required.
C=aha Public Power District Fort Calhoun Station Unit No. 1 Decket No. u5000235 an m r 3 vv-v0.,
Attach =ent No. 2
Corrective Action
Maintenance Order 3h06 was issued to = egger VA-33 fr0= the lead center and to check breaker trip settings.
The =otor meggered satis-factorily, however, the trip setting: for the A and C phases were found to be inaccurate and out-of-calibration as far as the long ti=e delay setting was concerned.
Consequently, two spare G.E. EC-2A trip units were installed as replacements in the breaker A and C phases.
The breaker was recalibrated and the trip setpoints were satisfactorily tested for proper operation. and the breaker was returned to service.
The contain=eni ecoling and recirculating fan, 7A-33 was prc=ptly returned to service and operated normally.
In addition, as a result of the failure of 7A-33, redundant c0=penents of the contain=ent cooling and recirculation system (in-cluding diesel D1) were tested for operability.
The following breakers for the equipment specified vere also tested (cycled) to ensure that their breakers vere operating satisfactorily:
SI-2A/23/2C H.P. SI ?u=ps SI-3A/33/3C Cent. Spray Pu=ps CH-1A/13/1C Charging Pumps 7A-3A Contain=ent Air ?.ecirculation 7A-TC/7D and Cccline Fan Units f?44'343 NOTT:
All equipment listed above contain breakers identical to that feeding 7A-33 All breakers operated satisfactorily.
However, during the re-dundant equip =ent operability testing of contain=ent cooling equip-
=ent, as required by Technical Specification 2.k. (1), HCV h033 failed to open fr0= the control *com switch HCV h033 is the 00=ponent ecoling vater inlet valve which supplies water to the cooling coil of the containment c0 cling fan VA-7D.
M.0. #3h07 vas written to correct this problem. As a result of this M.C.. it was discovered that a plugged Orifice in the pneu=atic controller of the valve was the source cf trouble.
The orifice vac repaired and the valve was i==ediately returned to service.
3cth incperable cc=ponents, VA-33 (breaker) and HCV h033 (pneunatic controller) were repaired and returned *.o operability within 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> which is within the 2h hour require =ent described by Technical Specification 2.a(2).
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Ctaha Public Power District Fort Calhoun Station Unit :To. 1 Oceket :To. 05000265 LZ?.30-001 Attachment Ifo. 3 Failure Data
~'his is the first failure of this type at the Fort Calhoun Station Unit :To. 1.
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1944 344
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| 05000285/LER-1980-001-03, /03L-0:800102,while Operating at Approx 98% Power, Breaker Feeding Containment Cooling Fan Motor VA-3B Tripped.Caused by Trip Units Out of Calibr.Units A&C Were Replaced,Calibr & Tested Satisfactorily | /03L-0:800102,while Operating at Approx 98% Power, Breaker Feeding Containment Cooling Fan Motor VA-3B Tripped.Caused by Trip Units Out of Calibr.Units A&C Were Replaced,Calibr & Tested Satisfactorily | | | 05000285/LER-1980-001, Forwards LER 80-001/03L-0 | Forwards LER 80-001/03L-0 | | | 05000285/LER-1980-002-01, /01T-0:on 800117,while Performing Surveillance Test ST-SI/CS-1,containment Sump Safety Injection Recirculation Valve HCV-383-4 Failed to Close from Control Room Switch.Caused by Binding Auxiliary Interlock | /01T-0:on 800117,while Performing Surveillance Test ST-SI/CS-1,containment Sump Safety Injection Recirculation Valve HCV-383-4 Failed to Close from Control Room Switch.Caused by Binding Auxiliary Interlock | | | 05000285/LER-1980-002, Forwards LER 80-002/01T-0 | Forwards LER 80-002/01T-0 | | | 05000285/LER-1980-003-03, /03L-0:on 800122,during Special 24-h Diesel Generator Test,While Attempting to Load Generator,Generator Field Went to Max Excitation.Caused by Faulty Zener Diode & Corresponding Draft in A-C Regulator Panel | /03L-0:on 800122,during Special 24-h Diesel Generator Test,While Attempting to Load Generator,Generator Field Went to Max Excitation.Caused by Faulty Zener Diode & Corresponding Draft in A-C Regulator Panel | | | 05000285/LER-1980-003, Forwards LER 80-003/03L-0 | Forwards LER 80-003/03L-0 | | | 05000285/LER-1980-004, Forwards LER 80-004/01T-0 | Forwards LER 80-004/01T-0 | | | 05000285/LER-1980-004-01, /01T-0:on 800126,while Fire Barrier Inside Empty Breaker Cubicle Was Degraded to Pull in New Cabling,Fire Watch Was Not Maintained Continuously.Caused by Fire Watch Not Receiving Accurate Info on Status of Barrier | /01T-0:on 800126,while Fire Barrier Inside Empty Breaker Cubicle Was Degraded to Pull in New Cabling,Fire Watch Was Not Maintained Continuously.Caused by Fire Watch Not Receiving Accurate Info on Status of Barrier | | | 05000285/LER-1980-005-03, /03L-0:on 800131,during Containment Integrated Leak Rate Test,Release to Atmosphere Occurred.Caused by Failure of Rupture Disk.Containment Pressure Monitored for Remainder of Test | /03L-0:on 800131,during Containment Integrated Leak Rate Test,Release to Atmosphere Occurred.Caused by Failure of Rupture Disk.Containment Pressure Monitored for Remainder of Test | | | 05000285/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000285/LER-1980-006-01, /01T-0:on 800415,as Required by IE Bulletin 79-01B,util Has Been Obtaining & Reviewing Test Data on Electrical Equipment.Samples Failed to Meet Acceptance Criteria.Caused by Steam & Moisture in Environ | /01T-0:on 800415,as Required by IE Bulletin 79-01B,util Has Been Obtaining & Reviewing Test Data on Electrical Equipment.Samples Failed to Meet Acceptance Criteria.Caused by Steam & Moisture in Environ | | | 05000285/LER-1980-006, Forwards LER 80-006/01T-0 | Forwards LER 80-006/01T-0 | | | 05000285/LER-1980-007-01, /01T-0:on 800430,penetration Cable Splices for Containment Ventilation Fans Found to Lack Documentation for LOCA Qualification.Splices Will Be Coated w/LOCA-qualified Sealant | /01T-0:on 800430,penetration Cable Splices for Containment Ventilation Fans Found to Lack Documentation for LOCA Qualification.Splices Will Be Coated w/LOCA-qualified Sealant | | | 05000285/LER-1980-007, Forwards LER 80-007/01T-0 | Forwards LER 80-007/01T-0 | | | 05000285/LER-1980-008-03, /03L-0:on 800515,during Check of Power Supply Trip Indicating lights,AB-1 Matrix Relay of Reactor Protective Sys Failed to Trip Clutch Power Supplies.Caused by Failure of Mercury Wetted Relay in Matrix Circuit | /03L-0:on 800515,during Check of Power Supply Trip Indicating lights,AB-1 Matrix Relay of Reactor Protective Sys Failed to Trip Clutch Power Supplies.Caused by Failure of Mercury Wetted Relay in Matrix Circuit | | | 05000285/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000285/LER-1980-009-99, /99T-0:on 800522,during Maint on Stack Iodine Process Monitor,New Sensitivity Calibr Was Required.Caused by Use of Wrong Calibr Procedure.Training Will Be Conducted to Ensure Familiarity W/Procedures | /99T-0:on 800522,during Maint on Stack Iodine Process Monitor,New Sensitivity Calibr Was Required.Caused by Use of Wrong Calibr Procedure.Training Will Be Conducted to Ensure Familiarity W/Procedures | | | 05000285/LER-1980-009, Forwards LER 80-009/99T-0 | Forwards LER 80-009/99T-0 | | | 05000285/LER-1980-010, Forwards LER 80-010/01T-0 | Forwards LER 80-010/01T-0 | | | 05000285/LER-1980-010-01, /01T-0:on 800516,during Cold Pressure Test,Leakage Discovered at Gasket Joint Between Pump Casing & Pump Cover on Reactor Coolant Pumps RC-3A,3B & 3C.Closure Studs Corroded by Boric Acid.Leaks Caused by Deteriorated Gaskets | /01T-0:on 800516,during Cold Pressure Test,Leakage Discovered at Gasket Joint Between Pump Casing & Pump Cover on Reactor Coolant Pumps RC-3A,3B & 3C.Closure Studs Corroded by Boric Acid.Leaks Caused by Deteriorated Gaskets | | | 05000285/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000285/LER-1980-011-03, /03L-0:on 800528,during 1980 Refueling Outage Type B & C Containment Leak Rate Tests,Total Leakage Exceeded 0.6La Limit.Caused by Leaking Fuel Transfer Tube, Electrical,Mechanical Sleeve & Piping Penetrations | /03L-0:on 800528,during 1980 Refueling Outage Type B & C Containment Leak Rate Tests,Total Leakage Exceeded 0.6La Limit.Caused by Leaking Fuel Transfer Tube, Electrical,Mechanical Sleeve & Piping Penetrations | | | 05000285/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000285/LER-1980-012-03, /03L-0:on 800708,during Performance of ST-RPS-3, F.2,discovered That Trip Unit 3 Setpoints Had Drifted Out of Spec in Nonconservative Direction.Caused by Normal Setpoint Drift.Setpoints Adjusted | /03L-0:on 800708,during Performance of ST-RPS-3, F.2,discovered That Trip Unit 3 Setpoints Had Drifted Out of Spec in Nonconservative Direction.Caused by Normal Setpoint Drift.Setpoints Adjusted | | | 05000285/LER-1980-013, Forwards LER 80-013/03L-0 | Forwards LER 80-013/03L-0 | | | 05000285/LER-1980-013-03, /03L-0:on 800707,during Normal Power Operation, Noted That Channel a Dc Sequencer SI-1 Had de-energized on-auto Light.Caused by Sequencer Circuitry Failure Due to Faulty Relay | /03L-0:on 800707,during Normal Power Operation, Noted That Channel a Dc Sequencer SI-1 Had de-energized on-auto Light.Caused by Sequencer Circuitry Failure Due to Faulty Relay | | | 05000285/LER-1980-014, Forwards LER 80-014/03L-0 | Forwards LER 80-014/03L-0 | | | 05000285/LER-1980-014-03, /03L-0:on 800709,transformer T4 of Diesel Generator 1 Failed.Caused by Shorted Coil.Transformer Replaced | /03L-0:on 800709,transformer T4 of Diesel Generator 1 Failed.Caused by Shorted Coil.Transformer Replaced | | | 05000285/LER-1980-015, Forwards LER 80-015/03L-0 | Forwards LER 80-015/03L-0 | | | 05000285/LER-1980-015-03, /03L-0:on 800710,during Insp,Noted That Trip Unit Setpoints on C Channel Had Become Positive Rather than Negative.Caused by Failure of 15-volt Power Supply for Trip Unit 4.Unit Calibr | /03L-0:on 800710,during Insp,Noted That Trip Unit Setpoints on C Channel Had Become Positive Rather than Negative.Caused by Failure of 15-volt Power Supply for Trip Unit 4.Unit Calibr | | | 05000285/LER-1980-016, Forwards LER 80-016/03L-0 | Forwards LER 80-016/03L-0 | | | 05000285/LER-1980-016-03, /03L-0:on 800621,weld on Suction Side of Pump CH-1B in Demineralized Water Flush Line Cracked.Caused by Vibration of Piping in Svc.Crack Was Ground Out & Rewelded Using Certified Procedure & Line Tested | /03L-0:on 800621,weld on Suction Side of Pump CH-1B in Demineralized Water Flush Line Cracked.Caused by Vibration of Piping in Svc.Crack Was Ground Out & Rewelded Using Certified Procedure & Line Tested | | | 05000285/LER-1980-017-03, /03L-0:on 800804,during Normal Power Operation, Personnel Discovered Setpoint Selector Switches for RMO-61, Particulate Radiation Monitor,In Wrong Position.Caused by Personnel Error While Performing Test on Radiation Monitor | /03L-0:on 800804,during Normal Power Operation, Personnel Discovered Setpoint Selector Switches for RMO-61, Particulate Radiation Monitor,In Wrong Position.Caused by Personnel Error While Performing Test on Radiation Monitors | | | 05000285/LER-1980-017, Forwards LER 80-017/03L-0 | Forwards LER 80-017/03L-0 | | | 05000285/LER-1980-018-03, /03L-0:on 800808,while Attempting to Monitor Gas Space on Vct,Inadvertent Release of Radioactive Matl to Auxiliary Bldg Environ Occurred.Caused by Deteriorated Surgical Tubing on Gas Analyzer.Tubing Replaced | /03L-0:on 800808,while Attempting to Monitor Gas Space on Vct,Inadvertent Release of Radioactive Matl to Auxiliary Bldg Environ Occurred.Caused by Deteriorated Surgical Tubing on Gas Analyzer.Tubing Replaced | | | 05000285/LER-1980-018, Forwards LER 80-018/03L-0 | Forwards LER 80-018/03L-0 | | | 05000285/LER-1980-019, Forwards LER 80-019/03L-0 | Forwards LER 80-019/03L-0 | | | 05000285/LER-1980-019-03, /03L-0:on 800904,seismic Pipe Restraints SIS-62 & SIS-7 Were Inadvertently Made Inoperable at Same Time. Restraints Were Being Upgraded in Response to IE Bulletin 79-14.Restraint SIS-7 Was Immediately Made Operable | /03L-0:on 800904,seismic Pipe Restraints SIS-62 & SIS-7 Were Inadvertently Made Inoperable at Same Time. Restraints Were Being Upgraded in Response to IE Bulletin 79-14.Restraint SIS-7 Was Immediately Made Operable | | | 05000285/LER-1980-020, Forwards LER 80-020/03L-0 | Forwards LER 80-020/03L-0 | | | 05000285/LER-1980-020-03, /03L-0:on 800905,axial Power Distribution Setpoints on D Channel Discovered Out of Tolerance in Nonconservative Direction.Caused by Dependent Setpoint Selection Switch Failure.Switch Cleaned & Returned to Svc | /03L-0:on 800905,axial Power Distribution Setpoints on D Channel Discovered Out of Tolerance in Nonconservative Direction.Caused by Dependent Setpoint Selection Switch Failure.Switch Cleaned & Returned to Svc | | | 05000285/LER-1980-021, Forwards LER 80-021/03L-0 | Forwards LER 80-021/03L-0 | | | 05000285/LER-1980-021-03, /03L-0:on 800910,transformer T4 of DG-1 Failed. Transformer Feeds Diesel Oil Immersion Heater & Alarm Relays.Caused by Moveable Armature Located on Immersion Heater Contractor.Armature Repaired | /03L-0:on 800910,transformer T4 of DG-1 Failed. Transformer Feeds Diesel Oil Immersion Heater & Alarm Relays.Caused by Moveable Armature Located on Immersion Heater Contractor.Armature Repaired | | | 05000285/LER-1980-022, Forwards LER 80-022/03L-0 | Forwards LER 80-022/03L-0 | | | 05000285/LER-1980-022-03, /03L-0:on 800911,during Safety Injection Actuation Signal Surveillance test,86B/VIAS Lockout Failed to Trip. Caused by Burned Coil.Coil Replaced W/Spare & Tested Satisfactorily for Proper Operation | /03L-0:on 800911,during Safety Injection Actuation Signal Surveillance test,86B/VIAS Lockout Failed to Trip. Caused by Burned Coil.Coil Replaced W/Spare & Tested Satisfactorily for Proper Operation | | | 05000285/LER-1980-023-03, /03L-0:on 800908,during Routine Operations,Power to Lockout Relay Coil 86A1/CPHS Was Interrupted.Caused by Electrically Opened Contacts.Contacts Cleaned & Burnished | /03L-0:on 800908,during Routine Operations,Power to Lockout Relay Coil 86A1/CPHS Was Interrupted.Caused by Electrically Opened Contacts.Contacts Cleaned & Burnished | | | 05000285/LER-1980-023, Forwards LER 80-023/03L-0 | Forwards LER 80-023/03L-0 | | | 05000285/LER-1980-024-03, /03L-0:on 800926,while Completing Repairs on B Charging Pump,A Charging Pump Became Inoperable.Caused by Packing Cooling Pump Failure.Motor Replaced | /03L-0:on 800926,while Completing Repairs on B Charging Pump,A Charging Pump Became Inoperable.Caused by Packing Cooling Pump Failure.Motor Replaced | | | 05000285/LER-1980-024, Forwards LER 80-024/03L-0 | Forwards LER 80-024/03L-0 | | | 05000285/LER-1980-025, Forwards LER 80-025/03L-0 | Forwards LER 80-025/03L-0 | | | 05000285/LER-1980-025-03, /03L-0:on 801027,during Power Operation While Completing Repairs on C Charging Pump,A Charging Pump Became Inoperable.Caused by Leak in Weld Joining Sys to Flushing Line.Weld Repaired & Pump Returned to Svc | /03L-0:on 801027,during Power Operation While Completing Repairs on C Charging Pump,A Charging Pump Became Inoperable.Caused by Leak in Weld Joining Sys to Flushing Line.Weld Repaired & Pump Returned to Svc | |
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