ML18152A156

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Insp Repts 50-280/89-08 & 50-281/89-08 on 890305-0401. Violations Noted.Major Areas Inspected:Plant Maint & Surveillance,Ler Review & Followup of inspector-identified Items
ML18152A156
Person / Time
Site: Surry  Dominion icon.png
Issue date: 05/02/1989
From: Fredrickson P, Holland W, Larry Nicholson, York J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A157 List:
References
50-280-89-08, 50-280-89-8, 50-281-89-08, 50-281-89-8, IEB-84-03, IEB-84-3, NUDOCS 8905190130
Download: ML18152A156 (22)


See also: IR 05000280/1989008

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

Report Nos.:

50-280/89-08 and 50-281/89-08

Licensee:

Virginia Electric and Power Company

Richmond, Virginia 23261

Docket Nos.:

50-280 and 50-281

Facility Name:

Surry 1 and 2

License Nos.:

DPR-32 and DPR-37

Inspection Conducted: March 5 through April 1, 1989.

Scope:

0n. ).

Inspector

J.

Inspector

te"si gned

SUMMARY

This routine resident inspection was conducted on site in the areas

of plant operations, plant maintenance, plant surveillance, licensee

event report review, and followup on inspector identified items.

A

special evaluation of the licensee 1 s program that was used to walk

down selected systems prior to unit restart was documented in the

last two resident inspector 1 s reports and this inspection effort

continues in this inspection report.

Certain tours were conducted on backshifts or weekends.

Backshift or

weekend tours were conducted on March 5, 11, 18, 26, 27, 28, 29, and

April 1, 1989.

Results:

During this inspection period, two violations were identified. The

first violation (paragraph 3.f(2)) concerns failure of the operators

to use procedures for realigning

CCW

and indicates that the

licensee 1 s corrective actions for past problems in the operations

area (reference NRC Inspection Report 280,281/88-51) has not been

entirely

effective

and

continues

to

require

additional

&9os 1 901 -.0

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_.,., 05000280

PDC

I

2

management attention.

The second violation contains three examples

of failure to meet the requirements of 10 CFR 50, Appendix B,

Criterion V.

These examples include problems

with

regard to

configuration control of instrumentation lines downstream of system

root valves (paragraph 4.a(2)), problems associated with returning

systems

to

service

after

modification

and/or

maintenance

(paragraph 4.b), and examples of inadequate instruction of personnel

performing inspection of cable splices indicating a lack of train~ng

and/or procedural guidance (paragraph 5.a).

One weakness was identified in paragraph 4.a(l) concerning an

apparent

lack of sensitivity to

harmful

contamination (i.e.

chlorides) on safety-related stainless steel piping .

REPORT DETAILS

1.

Persons Contacted

2.

Licensee Employees

  • W. Benthall, Supervisor, Licer.sing
  • R. Bilyeu, Licensing Engineer
  • R. Blount, Superintendent of Technical Services
  • D. Christian, Assistant Station Manager

D. Erickson, Superintendent of Health Physics

  • E. Grecheck, Assistant Station Manager
  • M. Kansler, Station Manager
  • J. McCarthy, Superintendent of Operations

G. Miller, Licensing Coordinator, Surry

J. Ogren, Superintendent of Maintenance

  • T. Sowers, Superintendent of Engineering

J. Price, Site Quality Assurance Manager,

Other licensee employees contacted included control room operators, shift

technical advisors, shift supervisors and other plant personnel.

  • Attended exit interview

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

Plant Status

The inspection period began with Units 1 and 2 in cold shutdown.

The

units remained in cold shutdown for the duration of the inspection period,

while substantial operational reviews and maintenance activities were

being conducted.

3.

Dperattonal Safety Verification (71707)

a.

Daily Inspections

The inspectors conducted daily inspections in the following areas:

control room staffing, access, and operator behavior; operator

adherence to approved procedures, technical specifications, and

limiting conditfons for operations; examination of panels containing

instrumentation and other reactor protection system elements to

determine that required channels are operable; and review of control

room operator logs, operating orders, plant deviation reports, tagout

logs, jumper logs, and tags on components to verify compliance with

approved procedures .

I J

b.

c.

2

During review of the control room logs, the inspectors noted that on

April 1, 1989, operators failed to properly align the flowpath to the

B boric acid transfer pump (1-CH-P-28) as required by OP 8.5.2, Batch

Mixing and Transfer to 1-CH-TK-18 Using 1-CH-P-28.

This condition

resulted in the pump being operated for approximately one minute

without a suction flowpath.

The operator recognized the error and

stopped the pump prior to pump damage occurring. The pump suction

valve was opened and the batching evolution was completed.

This

valve alignment discrepancy was properly identified to the control

room and a deviation report was submitted.

The nonlicensed operator

voluntarily submitted a detailed report to operations supervision

describing the event and how it could be prevented in the future.

The inspector considers that although the event had mininal safety

significance, the operator's response appears to indicate increased

sensitivity and accountability on the part of working level personnel

to identification of operational problems.

Weekly Inspections

The inspectors conducted weekly inspections in the following areas:

verification of operability of selected ESF systems by valve align-

ment, breaker positions, condition of equipment or components, and

operability of instrumentation and support items essential to system

actuation or performance. Plant tours were conducted which included

observation of general plant/equipment conditions, fire protection

and preventative measures,

control of activities in progress,

radiation protection controls, physical security controls, plant

housekeeping conditions/cleanliness,

and

missile hazards.

The

inspectors routinely monitored the temperature of the auxiliary

feedwater pump discharge piping to ensure steam binding is prevented.

Biweekly Inspections

The inspectors conducted biweekly inspections in the following areas:

verification review and walkdown of safety-related tagouts in effect;

review of sampling program (e.g., primary and secondary coolant

samples, boric acid tank samples, plant liquid and gaseous samples);

observation of control room shift turnover; review of implementation

of the plant problem identification system; verification of selected

portions of containment isolation lineups; and verification that

notices to workers are posted as required by 10 CFR 19.

d.

Areas Inspected

Inspections included areas in the Units 1 and 2 cable vaults*, vital

battery rooms, steam safeguards areas, emergency switchgear rooms,

diesel generator rooms, control room, auxiliary building, cable

penetration areas, independent spent fuel storage facility, low level

intake structure, and the safeguards valve pit and pump pit areas.

3

Reactor coolant system leak rates were reviewed to ensure that

detected or suspected leakage from the system was

recorded,

investigated, and evaluated; and that appropriate actions were taken,

if required.

The inspectors routinely independently calcuiated RCS

leak rates using the NRC Independent Measurements Leak Rate Program

(RCSLK9).

On a regular basis, RWPs were reviewed and specific work

activities were monitored to assure they were being conducted per the

RWPs.

Selec,ted :adiation protection instruments were periodically

checked, and equipment operabi 1 i ty and calibration frequency were

verified.

e.

Physical Security Program Inspections

In the course of monthly activities, the inspectors included a review

of the licensee's physical security program.

The performance of

various shifts of the security force was observed in the conduct of

daily activities to include: protected and vital areas access

controls; searching of personnel, packages and vehicles; badge

issuance and retrieval; escorting of visitors; and patrols and

compensatory posts.

f.

Licensee 10 CFR 50.72 Reports

(1)

(2).

On March 10, 1989, the licensee made a report in accordance with

10 CFR 50.72 with regards to questionable operability of the

Unit 1 inside recirculation spray pumps due to installation of

non original equipment manufacturer parts.

The parts had been

installed during the Unit 1 refueling outage in the summer of

1988.

This report was made after the licensee reviewed the

results of an engineering evaluation, which concluded that

operability of the pumps with these parts cannot be analytically

assured.

This issue was discussed in detail in NRC Inspection

Report 280,281/88-51.

In that inspection report, a followup

item was opened to monitor licensee evaluation of the issue.

However, additional NRC staff review of this issue resulted in

identification of an apparent violation in NRC Inspection Report

280,281/89-06.

On March 18, 1989, the licensee made a report in accordance with

10 CFR 50.72 with regards to increase in the Unit 1 RCS

temperature over a period of approximately 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> due to an

improper RHR system alignment.

This condition resulted in RCS

temperature increasing approximately 14 degrees F from 103F to

117F.

After correction of the system alignment problem, which

involved opening one valve to reestablish CCW flow through the

operating RHR heat exchanger, RCS temperature was reduced to

approximately 100 degrees F as desired for continuance of

maintenance evolutions.

The unit has been shut down since

September 14, 1988.

4

The sequence of events was as follows:

March 17, 1989 at approximately 10:00 p.m.

Operators were realigning the Unit 1 CCW system auxiliary loads

in containment from the A header to the 8 header in accordance

with a special test procedure.

RHR alignment at this time

consistec.1 of the A RHR pump running and providing RHR flow

through the A RHR heat exchanger.

The 8 RHR heat exchanger was

in normal alignment with its RHR discharge manual isolation

valve shut.

CCW flow into containment was through the A header

(A RHR heat exchanger).

CCW fl ow to the B RHR heat exchanger

was isolated by containment isolation valve TV-CC-1098 being

closed. TV-CC-1098 was closed as a result of the performance of

the special test.

During realignment of CCW auxiliary loads,

the operators realized that they would need to open the

TV-CC-1098 valve in order to reestablish CCW flow through the

CCW system auxiliary loads. This requirement was not identified

tn the special test procedure.

The operators bpened TV-CC-1098'

to reestab 1 i sh fl ow to the B CCW header.

They a 1 so shut the A

CCW

header containment isolation valve

TV-CC-109A.

When

TV-CC-109A was shut,

CCW to the A RHR heat exchanger was

secured.

With no

RHR water fl ow through the B RHR heat

exchanger, decay heat removal for the unit was secured.

March 17, 1989 - 10:00 p.m. to 12:00 a.m.

Shortly after realigning the system as described above, the

operators noticed a slow heat up rate on Unit 1; however, they

thought that the B header CCW manual throttle valve in contain-

ment needed adjustment and turned this condition over to the

oncoming midnight shift.

March 17, 1989 - 12:00 Midnight

Shift turnover to the midnight shift stated that the alignment

for decay heat removal on Unit 1 was through the B RHR heat

exchanger.

The turnover also indicated that a slow heatup was

in progress due to throttled CCW flow.

March 18, 1989 - Midnight to 8:00 a.m.

The midnight shift made a containment entry to increase CCW flow

through the B RHR heat exchanger and monitored the heatup

throughout the night.

March 18, 1989 - 8:00 a.m.

The oncoming day shift operators noticed that the unit

temperature was higher than it was the night before and

questioned other potential problems, including a possible valve

5

misalignment.

The operations superintendent also reviewed the

situation and directed that a containment entry be made to

verify valve alignment status for the RHR system.

March 18, 1989 - approximately 9:30 a.m.

The operators in containment verified that the discharge valve

for R~R flow through the B RHR heat exchang~r was shut.

The

operations supervisor directed that TV-CC-109A be reopened.

This evolution was accomplished and unit cooldown recommenced

when CCW flow was restored to the A RHR heat exchanger.

After the alignment deficiency was corrected, the licensee

stopped all abnormal evolutions and conducted a detailed review

of the event.

That review concluded that the swing shift had

realigned the CCW system as required by procedure during

recovery from a special test. However, the procedure being used

was not adequate to restore CCW flow through the B header. The

operators concluded that additional

valve operations were

necessary and performed these operations without the use of

procedures resulting in the loss of CCW fl ow through the

operating RHR heat exchanger.

The operators involved in this

evolution (Unit 1 RO and SRO) were not assigned to normal

control room shifts. They had been assigned to a control room

shift in order to satisfy the required time on shift to maintain

an active license.

Turnover to the midnight shift (which was

al so manned by an SRO not usually assigned to shift as a

licensed operator) identified a potential problem with regard to

a slow unit heatup; however, the operators initially thought

that this was due to inadequate CCW flow through the B RHR heat

exchanger, resulting in the oncoming shift continuing to monitor

the condition and adjust CCW flow to correct the problem.

All

attempted corrective actions involved containment entries to

operate manual

valves (average

containment

entry

takes

approximately 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />).

When the day shift arrived, it became

apparent that some other problem existed and a verification of

valve alignment for the CCW and RHR system valves was commenced.

This check confirmed that the RHR system was aligned with flow

i so.lated . through the B RHR heat exchanger.

The operators

immediately corrected the condition.

The inspectors monitored the licensee's actions with regard to

review of this event on March 18, and conducted an independent

review of the sequence of events.

The inspectors were a 1 so

present when licensee management was provided an overview of the

sequence of events by the operations staff.

The inspectors

noted that the licensee identified that several onshift

personnel during the time that the CCW system was improperly

aligned were not routinely assigned on shift. In addition, the

6

swing shift operators properly recognized a problem with flow

through the B CCW header; however, they failed to obtain a

procedure change prior to realigning the system.

Surry Technical Specification 6.4 requires that detailed written

procedures with appropriate check-off lists and instructions be

provided and followed for normal

startup, operation, and

shutdown of all systems and components involving nuclear safety

of the station.

Failure to properly realign the Unit 1 decay

heat removal system following testing is identified as a

violation of T~chnical Specification 6.4 (280/89-08-01).

The inspector noted that licensee management, including the

Station Manager and the Vice President - Nuclear, reported to

the station immediately after the event and conducted a review

to assess required immediate actions.

Licensee management is

continuing to maintain appropriate sensitivity to operational

events; however, additional actions are warranted to export this

sensitivity down to the working levels.

Within the areas inspected, one violation was identified.

4.

Operational Readiness Program Review (71710)

The inspectors continued to review the licensee's operational readiness

program as discussed in NRC Inspection Reports 280,281/88-51 and 89-06.

This .effort is. being performed in accordance with EWR 88-584, System

Review For Startup, and includes both field walkdowns and a review of

outstanding issues by the system engineers.

The resident inspectors are

routinely monitoring all aspects of this readiness program.

The following

details some specific inspection areas and findings from this review.

a.

Plant Configuration Confirmation

This portion of the program, performed in accordance with Attachment

u- to the above EWR,

consisted of the station system engineers

conducting field walkdowns of the systems and noting discrepancies

for resolution. These discrepancies were then evaluated to determine

if they should be corrected before unjt startup, and a justification

was written if deferral was recommend~d.

The inspectors continued to

monitor the licensee actions associated with this effort and

subsequently ide~tified the following concerns:

(1)

The inspectors independently walked down portions of the safety

injection and charging systems and noted a considerable amount

of paint on some of the systems' stainless steel piping. This

piping is located in and around the containment penetration area

of the auxiliary building basement and the paint appears to be

the result of inadequate protective techniques when the walls

and floor were painted.

7

Protective coatings used inside containment are procured per

Specification No. NUS-3003, which specifically prohibits the use

of coatings with water leachable chlorides.

Coatings used

outside containment, however, are procured per Specification No.

NUS-3004 and does not contain a requirement that the paint be

non-halogenated.

In

addition,

Section

C of

NUS-3004

specifically requires that stainless steel piping be protected

?rom paint.

A review of selected certificates of conformance

for paint recently used in the auxiliary building basement

indicates that the paint was supplied free of water leachable

chlorides, other halogens, and low melting point metals.

During the wa l kdown of the above systems by the app l i cab 1 e

system engineers, the engineers did not identify for evaluation

the paint on the stainless steel piping of safety-related

equipment. Although it appears that the paint being used in the

area is acceptable, the inspector expressed concern that an

apparent weakness exists regarding sensitivity to harmful

contamination of stainless steel pipe.

(2)

During the inspector's overview of the walkdown effort, a

concern was identified regarding the responsible organization

for operation and contra 1 of instrumentation va 1 ves.

Valve

operating checkoff procedure l-OP-7.lA, Engineering Safeguards-

Safety Injection System, was revised on December 23, 1988, to

delete the vent valves upstream of the safety injection

accumulator pressure transmitters from the valve checkoff list.

The reason stated for this deletion was that the vent valves

were removed when pressure transmitters were relocated by DC

87-01-1.

The subject vent_ valves (1-SI-401 through 406) were

in fact relocated along with the pressure transmitters versus

removal as stated on the procedure deviation. These valves are

located between the root isolation valves, upstream of the

reducer, and the transmitter isolation valve located at the

transmitter.

When questioned by the inspector, operations

personnel stated that these valves are under the cognizance of

the instrumentation shop and therefore do not belong in the

valve checklist.

The instrumentation shop subsequently denied

cognizance of these valves and stated that operations was

responsible for verifying proper alignment.

On March 27, the inspector met with the appropriate licensee

staff and concluded the following:

Valves associated with instrumentation are not consistently

depicted and labeled on station drawings and in the plant.

For example, the accumulator level transmitters are shown

on the station drawings with all the associated equalizing

and isolation valves, whereas other transmitters are shown

8

with no valves detailed or assigned numbers.

The licensee

stated that while this inconsistency has not caused a

previous plant operational problem, the situation has been

identified and will be addressed during the upcoming

component tagging upgrade program.

The licensee does not define in any procedure or document

the interface point between th Operations Department and

the Instrumentation Department regarding the operation and

position verification of valves.

For example a typical

instrumentation arrangement has a tee off the process line

with a normal sized root isolation valve.

Downstream of

this valve is a reducer down to tubing and a tubing run to

the instrument isolation valve that is just upstream of the

actual instrument.

The safety injection vent valves that

are discussed above are between the reducer and the

instrument isolation valve.

The Operations Department stated that it was their understanding

that they control up to and including the root isolation valve

that is just prior to the reduction down to instrumentation

tubing.

The Instrumentation Department stated that they control

only the instrument isolation valve that is immediately upstream

of the transmitter or sensor.

This informal understanding of

responsibilties as stated above means that valves and components

in the tubing between the two boundaries may not be adequately

controlled, and in fact, on December 23 1988, resulted in the

safety injection vent valves described above being deleted from

procedures.

The above item is identified as a violation

(280,281/89-08-02) of 10 CFR 50, Appendix 8, Criterion V, for

fa~lure to provide adequate instructions for control

of

instrumentation valves.

A subsequent verba 1 agreement was

reached among the licensee staff that the Instrumentation

Department would assume cognizance of all components dow~stream

of the reducer.

b.

Assessment of Oustanding Issues

This item is covered in Attachment IV to EWR 88-584 and includes a

review of oustanding temporary modifications and/or jumpers, station

deviations, commitment items, oustanding safety-related work orders,

_outstanding EWRs and open Type 1, 2, and 3 engineering evaluations.

The system engineers have been tasked with reviewing the above items

pertaining to their system and evaluating if closure of the item

should be performed prior to unit startup.

For those items that will

not be closed prior to startup, a justification for not completing

the item must be written and approved by the Superintendent of

Technical Services .

9

In addition to the above items for review, a revision to the EWR was

issued to require review of all

closed Type

1 engineering

evaluations.

A Type 1 study is the method used by the station to

request either the corporate design authority or any outside

engineering firm to perform an engineering analysis. A Type 2 study

is the conceptual engineering study that must be performed to support

a major plant design change, and a Type 3 document is the actual work

instructions to perform the modificaticn.

In the past, many Type 1

studies have been issued that made specific recommendations that the

plant should consider instead of proceeding to a major Type 2 study

and design change.

For these recommendations, the completed analysis

and recommendations would be sent to the Superintendent of Technical

Services and the Type 1 study would be classified as closed.

The

decision to

perform

subsequent corrective actions that were

recommended by the engineering study was at the sole discretion of

the Superintendent of Technical Services. The licensee realized that

approximately 620 closed Type 1 studies were on file with no

assurance that the necessary corrective actions were performed.

The

licensee stated that this situation was eliminated with the

January 1,

1989

reorganization of the

company 1 s

engineering

structure.

The inspectors reviewed the following closed Type 1 items and the

determinations for startup evaluation:

ST NP No. 1630, Control Room Habitability, Startup Issue

ST NP No. 1688, Evaluate Upgrade of the EOG Speed Sensing

Panels, Startup Issue (Type I closed, opened Type 3)

ST NP No. 1532, Control Room Habitability Evaluation (Charcoal

Filters), Startup Issue

ST NP No. 1584, Instrumentation for Main Control Room HVAC

System, Startup Issue

ST NP No. 1007, 35 KV Primary Feeder Cable To RSSTC, (Concerned

evaluation of different types of cable), Not A Startup Issue

ST NP No. 1065, Voltage Profile and Short Circuit Computer

Program, (No evaluation required, computer program has been

verified), ~ot A Startup Issue

ST NP No. 1149, Control Room Annnunciators, (Engin'eering Work

Request, Work Orders, and Technical Review Referenced), Not A

Startup Issue

10

The inspectors reviewed the following EWRs and the determinations for

startup evaluation:

EWR No. 89-94, Evaluate VS Strainer Piping (1-VS-S-18), Startup

Issue

EWR No.89-101, Evaluated Air Bottles in Mechanical Equipment

Room 3, Startup Issue

EWR No.89-122, Evaluate Ventilation Air Filter, Startup Issue

  • EWR

No.

86-457G,

Replacement

of

Control

Room

Chiller

(1-VS-E-4A),(Work Complete), Not a Startup Issue

  • EWR No.85-470, Eva 1 uate Upgrade of SA Line for Emergency

Switchgear Room, (Work Complete), Not A Startup Issue

  • EWR No. 86-288A, Evaluate Replacement of Exhaust Ducting in

System 1EL47, (Work Complete), Not a Startup Issue

Engineering determines *if a technical review must be performed before*

a system/component is returned to service.

Procedure SUADM-ENG-01,

dated November 3, 1987, paragraph 6.7.1 states in part, "If a

technical review is required, the system or component shall not be

considered operational until completion of the technical review."

The three asterisk marked items above indicate EWRs which work was

completed, but a technical review was not performed before the

system/component was returned to service. During the last inspection

period, URI 280/89-06-04 identified the fact that EWR No.88-440

(installation of high point vents) did not have a technical review

performed before the system was returned to service (Unit 1 only).

While a 11

EWR work performed does not require a change in the

drawing/procedure, the ex amp 1 e i dent ifi ed in the unreso 1 ved i tern

required changes in both areas.

The example in the URI along with

the failure to perform technical reviews for the three additional

EWRs above are identified as an example of violation 280,281/89-08-02

for failure to follow the procedure for performing technical reviews

before returning components/systems to service on Unit 1.

Other EWRs and closed Type 1 items reviewed were determined to be

acceptable.

c.

Inspection and [eview Status

The overall status of the engineering work as it pertains to Unit 1

as of March 28, 1989, was as follows:

Walkdowns

Total Items:

3332

Items Reviewed:

3076

Startup Items:

165

Commitments

Total Items:

743

Items Reviewed:

384

Startup Items:

79

11

Closed Type 1

Total Items:

631

Items Reviewed:

336

Startup Items:

6

EWRs

Total Items:

605

Items Reviewed:

51

Startup Items:

10

Open Type 1,2&3

Tota 1 Items:

261

Items Reviewed:

204

Startup Items:

56

Temp. Mods.

Total I terns:

16

Items Reviewed:

16

Startup Items:

5

Within the areas inspected, two violations were identified.

5.

Maintenance Inspections (62703)

During

the

reporting period,

the inspectors reviewed

activities to assure compliance with the appropriate

Inspection areas included the following:

a.

Evaluations of Motor Terminations

maintenance

procedures.

On March 9, the inspectors witnessed the lifting and inspection of

the motor leads for the auxiliary feedwater pump 2-FW-P-38. This work

was authorized on work order 78859 and was being performed in

accordance with EWR 89-148, Evaluate Misc. Motor Termination Quality,

dated February 23, 1989.

Previous inspection of the inside and

outside recirculation spray motors identified multiple installation

problems with the Raychem splice connection between the field cables

and the motor leads.

These problems included wrong sized and

improperly crimped lugs, damaged insulation, improper adhesion

materials and inadequate substrate length. The purpose of the above

EWR is to assure that these problems do not extend to other motors.

The inspection effort included witnessing the removal of the Raychem

and the subsequent inspection and documentation of the results.

These results were forwarded to design engineering for a fi na 1

_assessment of w~ether the quality of the terminations is acceptable

or require repairs.

Specific discrepancies noted on the 2-FW-P-38 motor were as follows:

Lugs connected back. to back resulting in maximum conductor

misalignment

Bolts were 1 inch long, resulting in sharp protrusion *Of splice

and excessive stretching of Raychem covering material

12

Breakaway torque of connecting bolts was only 4 to 5 ft-lbs

Lugs on field cable were 600V instead of 5kV

Damaged field lug from torquing against smaller motor lug

The above discrepancies were reported on station deviation S2-89-276,

dated March S, 1989.

The inspector noted during the witnessing of

the inspection that the entire Raychem (shims) was not removed.

The

discussion section of the above EWR states that the Raychem will be

completely removed on all motors in environmentally harsh areas. The

AFW motors are located in the steam side of the safeguards area which

is susceptible to a steam line break.

The licensee agreed that the

entire Raychem should have been removed and subsequently completed

its removal. The inspector considers that additional guidance should

have been provided to specify classification of environments in order

to ensure appropriate inspections are conducted.

This item is an

example of a lack of adequate instruction for the inspection of motor

terminals.

Attachment II, Record 48 of EWR 89-148, contains the procedure for

removal, inspection and retermination of the motor leads for

  • 2-FW-P-38.

On March 28, 1989, the inspector reviewed the official

copy of this procedure and discovered a problem with the method of

documenting and resolving the discrepancies. Specifically, step 1.4

of this procedure was signed by the design engineer and a sketch was

incorporated specifying the requirements for retermination of this

connection.

The next step (step 1.5) directs the craft to

reterminate the cable in accordance with the generic station Raychem

instructions and the sketch provided in the previous step.

The

sketch that was included by the design engineer did not adequately

address the deficiencies noted during the 'as found' inspection (i.e.

600V lugs) and was incorporated into the procedure without any review

process. The actions taken by the design engineer appears to be in

compliance with the EWR as it is currently written. The end result

is that a single individual can issue instructions to disposition

defects and assemble a field connection without prior review or

approval.

The licensee agreed with the inspector's findings and

placed an. engineering hold on the EWR until the problem is reviewed

and resolved.

This item, as well as the example discussed above,

are identified as one example of violation 280,281/89-08-02, for

failure to provide adequate instruction for inspection of motor

terminals.

-

b.

Evaluation of Training For Installation of Raychem Electrical

Insulation Kits

The inspectors attended a training session for the electrical craft

in regards to the installation of Raychem kits.

These heat

shrinkable components are installed over electrical cable bolted

splices for (1) mechanical protection, (2) electrical insulation, and

as only 4 to 5 ft-lbs

of SkV

t smaller motor lug

ation deviation S2-89-276,

during the witnessing of

ims) was not removed.

The

that the Raychem will be

,mentally harsh areas. The

f the safeguards area which

e licensee agreed that the

.nd s*ubsequently completed

additional guidance should

on of environments in order

inducted.

This item is an

for the inspection of motor

contains the procedure for

f the motor leads for
tor reviewed the official

p

with the method of

e

ecifically, step 1.4

n e ,neer and a sketch was

for retermination of this

directs the craft to

the generic station Raychem

the previous step.

The

~ngineer did not adequat:lY

, *as found' inspection (1.e.

  • procedure without any rev~ew

, engineer appears to be ,n

tly written. The end r~sult

nstructions to cfisposition

n without prior review or

~ inspector 1 s'findings and

ntil the problem is reviewed

e example discussed above,

1 t; on 280, 281/89-08-02, for

., for inspection of motor

ion of Raychem Electrical

sion for the electrical craft

~a-

kits.

These heat

,e

ctri cal cab 1 e bo 1 ted

(

ectrical insulation, and

13

1t moisture.

The course was conducted by a Raychem

and a licensee electrical engineer.

The training

1ychem basic installer/inspector course, which included

of what heat shrinkable tubing is and how it is made.

were various installation techniques and potential

removal

of the tubing after installation.

The

ed that most problems encountered in the field are not

perforr.1ance, but to misapplication of the ~aychem

ture,

smaller groups

performed actual

Raychem

ing training kits.

The groups were then required to

chem material

from

the electrical cables.

The

rved various groups and their techniques during the

1ing. The inspectors noted by discussions with three

in the training class that they had used Raychem

in the field numerous times.

was made by a licensee electrical engineer regarding

  • oblems associated with Raychem applications on

,nents found at Surry. The groups were informed to be

rt any of these conditions.

The engineer also

,f the requirements in procedure NUS 2030, Specifica-

  • ical Installation, and noted several areas where

1ractices varied from the Raychem instructions.

The

der that the training was accomplished in an adequate

1aintenance/Modification On

The

Low Head Safety

currently removing the Unit 1 low head safety

-SI-P-lA in order to r~place the replica parts (non

nt manufacturer parts) previously placed in the

ector reviewed procedure MMP-P-C-SI-090, Remova 1,

pection, Repair, Reassembly, and Reinstallation of

Injection Pump

11Safety -Related", dated August 20,

and signed off portions of this procedure were

spector attended two of the pre-job briefings held

e team performing this job.

_ 1d, part of the column and part of the shaft have

1 the pump well.

The inspectors will follow the

?maining parts, including removal of the two stage

TI of the well, and observe the replacement of the

ing the next inspection period.

iected, additional examples of a violation were

14

6.

Surveillance Inspections (61726)

During the reporting period, the inspectors reviewed various surveillance

activities to assure compliance with the appropriate procedures as

fo 11 ows:

Test prerequisites were met.

Tests were performed in accordance with approved procedures.

Test procedur2s appeared to perform their intended function.

Adequate coordination existed among personnel involved in the test.

Test data were properly collected and recorded.

Inspection areas included the following:

a.

Containment Spray Check Valves

The inspector reviewed periodic test 1-PT-17.4, Containment Spray And

Recirculation Spray Check Valves, dated February 16, 1989.

This

surveillance

procedure,

performed

during

refueling

shutdown

conditions, implements the requirements of Technical Specification

paragraph 4. 5. A. 4 that each weight 1 oaded check va 1 ve within the

containment be tested to verify capability to open by pressurizing

upstream and verifying air flow through the check valve.

In

addition, verification of seating of the check valves is accomplished

by applying a vacuum upstream of the valves and verifying no air

flow.

The inspector discussed the test method with the operations staff

that performs the test, as we 11

as the appropriate cognizant

engineer, and expressed concern that the test procedure was not

specific as to which rotameter to use when verifying the presence or

absence of flow.

The procedure requires that an air test rig with a

rotameter be in sta 11 ed upstream of the valve to be tested and a

rotameter to be installed downstream of the valve.

The procedure

step that verifies flow states: "Note the flow on the rotameter when

the check valve lifts".

The use of the rotame.ter installed on the

test rig may not provide positive verificatio*n that air flow is

passing through the check valve in lieu of leaking out an unknown

path in the maintenance boundary.

Discussions with operational

  • -personnel that have performed the test indicate that the common

practice is to use the downstream rotameter.

The system engineer

concurred and agreed to clarify the test procedure.

No additional

discrepancies or outstanding concerns were noted.

b.

15

Special Test 242, Unit 1 B Train Bus Deactivation Test

During the week of March 13 - 17, 1989, the inspectors witnessed

performance of ST-242.

The purpose of the test was to systematically

deenergize the Unit 1 J bus and to verify that B train components are

powered by the lJ bus.

The inspectors monitored performance of

testing from the control room including discussions with the test

di rector and unit SROs.

The contra 11 i ng procedure was frequer.t ly

reviewed during test performance.

The inspectors noted th~t the test

evolutions were being properly controlled and that unit status was

not adversely affected.

No discrepancies were noted.

c.

Flowtesting of the Unit 2 Inside Recirculation Spray Pumps

The inspector reviewed ST-233, Operability of IRS Pumps, which was

issued and approved on December 2, 1988.

The purpose of the test is

to measure pump flow, system pressure, and motor current over a range

of different fl owrates, and to evaluate these recorded parameters

against pump data associated with the manufacturers pump curves.

This engineering evaluation will establish pump operability status as

well as setting reference values for the IRS pumps in accordance with

Section XI of the ASME code.

The inspector reviewed the initial

conditions, precautions, and instrumentation requirements listed in

the test as well as the actual performance steps.

The inspector

identified the following test procedure weaknesses to the licensee:

Provide a means for monitoring of containment sump water

temperature.

This requirement is based on precaution 4.2 which

states that the temperature of the sump water should remain

below 120 degrees F for personnel protection.

Add steps that verify remova 1 of cleanliness covers from the

system I s permanent spool pieces and piping prior to their

reinstallation.

The licensee incorporated the above items into the test procedure.

The inspector conducted a walkdown of the 8 inch flow test line in

the Unit 2 containment and verif.ied that the pressure gages and

flowmeter calibration were withfn the required frequency.

The

inspector noted that the test line valves were not tagged with their

_respective va 1 ve numbers.

The licensee test di rector stated that

these va 1 ves would be properly tagged prior to test performance.

A

subsequent inspection verified proper tagging of the test valves.

ST-223 was initiated on March 23, 1989, and the inspector witnessed

system alignment, filling .and venting of the test instrumentation,

and initial pump operation. However, during the test, the flowmeter

exhibited large fluctuations .such that meaningful flow data could not

be obtained. The test was secured to resolve the flowmeter problem.

Additional test monitoring was not accomplished for this test during

this inspection period.

16

Within the areas inspected, no violations or deviations were identified.

7.

Licensee Event Report Review (92700)

The inspectors reviewed the LERs listed below to ascertain whether NRC

reporting requirements were being met and to determine appropriateness of

the corrective actions. The inspector's review also included followup on

implementation of corrective action and review of licensee docum~ntation

that all required corrective actions were complete.

LERs that identify violations of regulations and that meet the criteria of

10 CFR, Part 2, Appendix C,Section V are identified as LIV in the

following closeout paragraphs.

LIVs are considered first-time occurrence

violations which meet the NRC Enforcement Policy for exemption from

issuance of a Notice of Violation.

These items are identified to allow

for proper evaluations of corrective actions in the event that similar

events occur in the future.

(Closed) LER 280/88-17, Debris in Containment Sumps Due to Inadequate

Inspection Program.

The issue involved licensee identification of foreign

material which was discovered in the Unit 1 containment sump during pump

testing.

Licensee corrective action included cleaning of the sumps and

associated piping.

In addition, the licensee instituted improvements to

their foreign material exclusion program to prevent recurrence.

This

i~sue resulted in enforcement action which was discussed in NRC Inspection

Report 280,281/88-28.

This LER is closed.

(Closed)

LER 280/88-18, Personnel Overexposure.

The issue involved

exposure to a contract employee of radiation in excess of the quarterly

limit as specified in 10CFR20.

Corrective action for this condition

included enhancements to the radio l ogi cal protection program at the

station. This issue resulted in enforcement action which was discussed in

NRC Inspection Report 280,281/88-25.

This LER is closed.

(Closed) LER 280/88-22, Unit Rampdown to Cold Shutdown Due to MOV-CS-1018

...Leakage.

The issue involved leakage past a containment isolation valve

when Unit 1 was at intermediate shutdown conditions.

The unit was

returned to the cold shutdown condition as required by Technical

Specifications and repairs were made to the subject Vijlve.

The inspector

verified that the valve repairs were comp 1 eted and that the va 1 ve was

properly retested. This LER is closed.

(Closed) LER 280/88-19, Reactor Trip/Safety Injection Due to Spurious Hi

CLS Signal as a Result of a Malfunctioning Relay.

The issue involved a

reactor trip/safety injection of Unit 1 from 100 percent power.

The trip

was caused by a failed relay.

The relay was replaced and satisfactorily

tested.

The inspector reviewed the post-trip report and monitored

licensee SNSOC actions prior to restart.

This LER is closed.

I

I

17

(Closed) LER 280/88-31, Potential for an Inadequate Service Water Supply

During a LOCA with a Loss of Offsite Power.

The issue involved the

licensee's review of the design bases of the Service Water System.

During

that review several deficiencies were identified which required corrective

actions prior to unit restart.

The corrective actions have been

identified and are ongoing.

This issue resulted in enforcement action

which was discussed in NRC Inspection Report 280,281/88-32.

Th.;s LER is

closed.

(Closed) LER 280/88-32, Potential for Overload of EDGs During a LOCA with

LOOP Due to Design Deficiency.

This issue involved the licensee's review

of a design deficiency associated with potential overload of the EDGs

during a design bases accident followed by a LOOP.

The licensee placed

the operating unit in cold shutdown and has subsequently modified the

emergency busses to a 11 ow for appropriate sequential loading of these

buses in the worst case scenario.

The inspector reviewed the licensee's

LER and has monitored licensee corrective actions and testing.

This LER

is closed.

(Closed) LER 280/88-33, Main Control Room Envelope AC System Inadequate.

This issue involved the licensee's review of present capacity of the

subject system based on initial evaluation of system test results which

were conducted in the Fall 1988.

Testing concluded that the system would

not perform its design function.

Corrective actions included design

changes and refurbishment of the present system for interim use.

Additional long term corrective action will include development and design

of new equipment.

The inspectors will continue to monitor the licensee's

interim and long term corrective actions.

This issue resulted in

enforcement action which was discussed in NRC Inspection Report 280,

281/88-41.

This LER is closed.

(Closed) LER 280/88-40, Accumulation of Gases in Suction Piping of HHSI

Pumps Due to Inadequate Design.

The issue involved potential accumulation

of gases in the suction piping of both units' HHSI pumps.

Corrective

-action* included installation of high point vents in the suction lines for

each unit.

The inspector verified that the high point vents were

installed as specified.

This issue resulted in enforcement action which

was discussed in NRC Inspection Report.280,281/88-41.

This LER is closed.

(Closed) LER 281/88-05, Inoperable Control Rods Due to Failed Phase

Control Cards.

The issue involved a failure of the rod control system

requiring initiation-of a unit ramp to shutdown conditions as required by

Technical Specifications.

Licensee corrective actions included repairs to

the rod control system and testing to confirm operability.

Testing was

accomplished satisfactorily; however, this issue resulted in enforcement

action which was discussed in NRC Inspection Report 280,281/88-11. This

LER is closed .

J

18

(Closed) LER 281/88-06, Fail~re to Comply with Technical Specification Due

to Personnel Consideration.

The issue involved failure to post a fire

watch in the Unit 2 containment within Technical Specification time

requirements while the unit was at full power.

Corrective action included

alternate monitoring for a containment fire. Additional corrective action

included submittal of a Technical Specification change ,to allow for

alternate monitoring for a fire. The inspector verified that the licensee

prerared a Technical Specification change which was consistent with

requirements of other similar plants.

This LER is closed.

(Closed) LER 281/88-08, Inadequate Boric Acid Flowpaths Due to Personnel

Error and Inadequate Procedures.

The issue involved a loss of boric acid

flowpath to the suction of the charging pumps in violation of Technical

Specification 3.2.B.4.

The cause of this violation was personnel error

and inadequate procedure.

Corrective actions included a procedure

revision to provide for proper system alignments. The inspector verified

that the procedure revisions were accomplished and appropriate operator

training was conducted .. This item is identified as a LIV (281/89-08-03)

for failure to provide adequate procedure to ensure

Technical

Specifications are complied with.

This LER is closed.

(Closed) LER 281/88-10, Reactor Trip Due to Low Low Steam Generator Level

Due to Closure of Turbine Governor Valves.

The issue involved a Unit 2

reactor trip from full power due to a valid steam generator low low level

signal.

The cause of the valid trip signal was rapid closure of the

turbine governor valves. Licensee actions after the trip and appropriate

inspector followup were discussed in NRC Inspection Report 280,281/88-18.

This LER is closed.

(Closed) LER 281/88-24,

11A

11 and

118

11 Inside Recirculation Spray Pumps Found

with Internal Damage.

The issue involved discovery of internal damage to

the subject pumps during refurbishment.

Licensee corrective actions

included overhaul of the pumps.

In addition, full flow testing will be

conducted on these pumps during each refueling outage to prove continued

operability. The inspectors reviewed the licensee actions and witnessed

IRS pum*p testing.

This LER is closed.

(Closed) LER 281/88-25, LHSI

Pump Discharge MOVs 2863A and B Power

Sup.plies Interchanged. The issue involved licensee determination that the

subJect valves were powered from the wrong train power supply.

Licensee

corrective action included correcting the power supply discrepancy.

In

addition, an extensive test program was instituted to determine if any

additional problems of this nature existed.

The inspectors monitored

licensee corrective actions and evaluations in this area.

This issue

resulted in enforcement action which was discussed in NRC Inspection

Report 280,281/88-45.

This LER is closed.

19

8.

Action on Previous Inspection Findings (92702)

(Closed) URI 280/89-06-04, Requirements for Returning Safety-Related

Syst~ms to Service After Maintenance or Modification. This item involved

additional review of the l icensee 1 s program which requires a technical

review of modifications to systems prior to returnin§ to service.

Additional reviews were conducted by the inspector during this period and

are addressed in paragraph 4.b.

This URI is closed.

(Reinspected/Closed) IE Bulletin 84-03, Refueling Cavity Water Seal.

The

licensee's January 9, 1989 revised response to IE Bulletin 84-03 provided

additional corrective actions with regard to the reactor cavity seal

assembly.

These corrective actions have been verified, as documented in

NRC Inspection Reports 280,281/88-38 and 88-47, and this item is closed.

9.

Exit Interview

The inspection scope and findings were summarized on April 4, 1989, with

those individuals identified by an asterisk in paragraph 1. The following

new items were identified by the inspectors during this exit:

One violation (paragraph 3.f(2)) was identified regarding a failure to

provide and/or follow procedure involving startup, operation, and shutdown

of systems and components involving nuclear safety of the station

(280/89-08-01).

One violation, with three examples, was identified for failure to meet the

requirements of 10 CFR 50, Appendix B, Criterion V (280,281/89-08-02).

The examples included failure to provide adequate procedures for the

operation and control of instrumentation valves (paragraph 4.a.(2)),

failure to follow procedure for performing technical reviews before

returning components/systems to service (paragraph 4.b), and failure to

provide adequate instructions for the inspection and retermination of

motor connections (paragraph 5.a).

_One weakness was identified_ (paragraph 4.a.(l)) concerning an apparent

lack of sensitivity. to harmful contamination (i.e. chlorides) on safety

related stainless steel piping.

The licensee acknowledged the in"spection findings with no dissenting

comments.

The licensee did not identify as proprietary any of the

materials provided to or reviewed by the inspectors during this

insp-ection.

10.

Index of Acronyms and Initialisms

AFW

AP

cc

ccw

AUXILIARY FEEDWATER

ABNORMAL OPERATING PROCEDURE

COMPONENT COOLING

COMPONENT COOLING WATER

20

CFR

CODE OF FEDERAL REGULATIONS

CW

CIRCULATING WATER

DC

DESIGN CHANGE

DP!

DELTA PRESSURE INDICATORS

DR

DEVIATION REPORT

EOG

EMERGENCY DIESEL GENERATOR

EMP

ELECTRICAL MAINTENANCE PROCEDURE

ESF

ENGINEERED SAFETY FEATURE

ESW

EMERGENCY SERVICE WATER

EWR

ENGINEERING WORK REQUEST

HX

HEAT EXCHANGER

HPSI

HIGH PRESSURE SAFETY INJECTION

IE

INSPECTION AND ENFORCEMENT

IF!

INSPECTOR FOLLOWUP ITEM

IRS

INSIDE RECIRCULATION SPRAY

!SI

INSERVICE INSPECTION

LER

LICENSEE EVENT REPORT

LIV

LICENSEE IDENTIFIED VIOLATIONS

LHSI

LOW HEAD SAFETY INJECTION

LOCA

LOSS OF COOLANT ACCIDENT

LOOP

LOSS OF OFFSITE POWER

MOV

MOTOR OPERATED VALVE

NRC

NUCLEAR REGULATORY COMMISSION

NRR

NUCLEAR REACTOR REGULATION

OP

OPERATING PROCEDURE

PI

PRESSURE INDICATOR

PM

PREVENTATIVE MAINTENANCE

PSI

POUNDS PER SQUARE INCH

PSIG

POUNDS PER SQUARE INCH GAUGE

PT

PERIODIC TEST

QA

QUALITY ASSURANCE

QC

QUALITY CONTROL

RCS

REACTOR COOLANT SYSTEM

RHR

RESIDUAL HEAT REMOVAL

RO

REACTOR OPERATOR

RPS

REACTOR PROTECTION SYSTEM

RSS

RECIRCULATION SPRAY SYSTEM

RWP

RADIATION WORK PERMIT

SI

SAFETY INJECTION

SNSOC

STATION NUCLEAR SAFETY AND OPERATING COMMITTEE

SRO

SENIOR REACTOR OPERATOR

SW

SERVICE WATER

TS

TECHNICAL SPECIFICATIONS

URI

UNRESOLVED ITEM

VS

  • VENTILATION SYSTEM

TSC

TECHNICAL SUPPORT CENTER