ML18086B002

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IE Insp Repts 50-272/81-23 & 50-311/81-21 on 810804-0914. Noncompliance Noted:Failure to Comply W/Tech Spec Requirements Prior to Mode Change & Failure to Perform Periodic Surveillances
ML18086B002
Person / Time
Site: Salem  PSEG icon.png
Issue date: 10/06/1981
From: Greenman E, Hill W, Norrholm L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML18086A999 List:
References
50-272-81-23, 50-311-81-21, NUDOCS 8111050602
Download: ML18086B002 (23)


See also: IR 05000272/1981023

Text

-

f

I

U. S. NUCLEAR REGULATORY COMMISSION

OFFICE OF INSPECTION AND ENFORCEMENT

(DCS Numbers - see

attached sheet)

Report Nos.

Docket Nos.

License Nos.

Licensee:

50-272/81-23

50-311/81-21

50-272

50-311

DPR-70

DPR-75

REGION I

Public Service Electric and Gas Company

80 Park Plaza

Newark, New Jersey

07101

F ac i 1 i ty Name : __

s_a_l e.;._m.;_,.;;N.;..;.uc.;._l..;.:.e..;.:.a.;_r ""'"'G..;.:.e..;.:.n.;;;..er..;.:.a..;.:.t...;..i .;.;.,ng~S....:;.t.;;;.a t.;;_i....:;.o..;.:.n_-_...;.U..;.:.n...:..i t.::..;s;._;;;,1-'a;;;,;.n,;..;.d;....,;;;.2 _

Inspection At: __

H_a_nc_o_c_k_s _B_r_i .....

dg..._e_..,_Ne_w_Je_r_s_e ....... Y ________ _

1981

Inspectors:

L.

  • orrholm,

~m./M1)*

W. M. Hill, Jr., Resident Reactor Inspector

Approved By:

Uwa/_/lJl~

E. G. Greenman, Chief, Reactor Projects Section No. 2A,

Projects Branch No. 2, DRPI

SEP 2 8 1981

date

SEP 2 8 1981

date

_1of6if;

d'ate

Inspection* Summary:

. ';:'..

Inspections* on* August* 4 *..;*September *14; 19.81 * (Comolnea *Report* Numbers* 50.:.212/81.:..23

and 50-311/81.:..lll

Unit 1 Areas* Irisaected: Routine inspections 5y the resident inspectors*#of plant

operations incl u mg tours of the facil i'ty; conformance wi.tfl Technical Specifica-

tions and operatfng parameters; log and record review; reviews of licensee events;

and followup on prevfous inspection items.

The inspection involved 68 inspector-

flours 5y the resident NRC inspectors.

Results:

Two items of noncompliance were identified (Failure to comply with

Technical Specification requirements prior to mode changes - paragraph 6; failure

to perform periodic survei.11 ances - paragraph 3}.

Unit 2 Areas Ins~ected: Routine inspections by the resident inspectors of plant

startup testing including tours of the facility; conformance with 1 icense require- .

ments and Technical Specifications; and reviews of licensee events; and followup

on previous inspection items.

The inspection involved 84 inspector-hours by the

resident NRC inspectors.

Results: Three items of noncompliance were identified (Failure to comply with

Technical Specification requirements prior to mode changes - paragraph 6; failure

to comply with a license': condition - paragraph 7, failure to perform periodic

surveillances- paragraph 3).

( 8111050602 811007

1

1

PDR ADOCK 05000272

G

PDR

\\

I

Report Nos. 50-272/81-23 and 50-311/81-21

DCS Nos *

050272-810910

050272-810902

050272-810810

050272-810414

050272-810404

050272-810422

050272-810220

050272-810426

050272-810505

050272-810506

050272-810429

050272-810512

050272-810513

050272-810514

050272-810518

050272-810501

050272-810520

050272-810521

050272-810526

050272-810528

050272-810616

050272-810612

050272-810616

050272-810621

050272-810715

050272-810624

050272-810628

050272-810703

050272-810626

050311-810810

050311-810822

050311-810829

050311-810831

050311-810902

050311-810903

050311-810911

050311-810419

050311-810407

050311-810423

050311-810426

050311.,8l0427

050311-810501

050311-810505

050311-810430

050311-810515

050311-810517

050311-810519

050311-810520

050311-810522

050311-810523

050311-810603

050311-810526

050311-810530

050311-810601

050311-810603

050311-810616

050311-810606.

050311-810608

050311-810623.

050311-810608

050311-810609

050311-810612

050311-810618

050311-810707

050311-810423

050311-810622

050311-810623

050311-810625

050311-810626

050311-810625

050311-810627

050311-810701

' .

~

I

L

.. DETAILS

I. Persons Contacted

J. Driscoll, Chief Engineer

L. Fry, Station Operating Engineer

J. Gallagher, Assistant Maintenance Engineer

S. LaBruna, Maintenance Engineer

H. Midura, Manager - Salem Generating Station

L. Miller, Station Performance Engineer

F. Schnarr, Reactor Engineer

R. Silverio, Assistant to the Manager

J. Stillman, Station QA Engineer

R. Swetnam, Radiation Protection Engineer

The inspector also interviewed and talked with other licensee personnel

during the course of the inspections including management, clerical,

maintenance, operations, performance and quality assurance personnel.

2.

Status of Previous Inspection Items

(Closed) Follow Item (272/80-32-04).

Inclusion of IE Circular 80-18

considerations relative to design changes in EDD-1.

The inspector

reviewed EDD-1, Operational Design Change Control, Revision 3,

approved on March 30, 1981. All considerations listed in IEC

80-18 have been incorporated both by reference and by inclusion

of the Circular in the procedure.

The inspector had no further

questions on this item.

(Closed) Unresolved Item (272/81-14-01}. Technical Specifications for

mechanical snubber surveillance.

By correspondence dated August

10, 1981, the licensee requested a change to the Technical Speci-

fications regarding testing of mechanical snubbers.

The proposed

format appears consistent with Standard Technical Specifications

on this subject. The inspector had no further questions on this

item.

(Closed) Noncompliance (272/81-01-03). Failure to post in accordance with

10 CFR 19. Revision 5 to Administrative Procedure 16, Posting

of Regulatory Material, was issued on July 16, 1981. This pro-

cedure establishes responsibilities and official bulletin boards

along worker access routes for the posting of material in accor-

dance with 10 CFR 19. The inspector also confirmed that an item

of noncompliance relating to radiological health identified in

Inspection Report 50-272/81-22 had 6een appropriately posted.

The

inspector f:iad no further questions on this item.

lCl osed }_

Fo 11 ow Item (311/81-10-01}.

Review deta i 1 s of April 23, 1981

safety injection. This event, reported as LER 50-311/81-45/99X

is reviewed in this report. The inspector had no further questions *

(Closedl

(Open).

SITE

3

Noncompliance (272/80-06-02}. Exceeding steady state power limit.

The inspector reviewed Operating Memorandum 6, Guidelines For

Operation at 100 % Power, dated June 23, 1981.

Instructions for

maintaining average power and absolute limits for indicated thermal

power are provided.

The guidelines are consistent with NRC direc-

tion provided in this area.

No recurrence of this item has been

identified. The inspector had no further questions.

Noncompliance (272/80-31-01}. Failure to comply with administra-

t1ve procedures with respect to procedure periodic reviews. The

inspector noted that licensee activities to revise and upgrade

procedures are continuing with most in the final stage of prepara-

tion and review.

The inspector further noted that the requirements

of Administrative Procedure 3, Document Control Program, were not

being met. Specifically, on-the-spot changes are required, by

AP-3, to be incorporated into a revision within six months.

The

licensee stated that this is an unreasonable interval and that a

revision will be initiated to AP-3 in support of a more workable

system. Resolution of this interval is a new unresolved item

(272/81-23-07}.

3. Shift Logs and Operating Records

a.

The inspector reviewed the following plant procedures to determine the

licensee established requirements in this area in preparation for a

review of selected logs and records.

AP-5, Operating Practices, Revision 10, May 21, 1980;

AP-6, Operational Incidents, Revision 6, February 22, 1979;

AP-13, Control of Lifted Leads and Jumpers, Revision 4, February

11, 1980;

Operations Directive Manual; and,

AP-15, Safety Tagging Program, Revision 1, November 21, 1980.

o. Shift logs and operating records were reviewed to verify that:

.

--.

~

Control room log sheet entries are filled out and initialled;

Auxiliary log sheets are filled out and initialled;

Log entries involving abnormal conditions provide sufficient

detail to communicate equipment status, lockout status, correction

and restoration;

Log book reviews are befog conducted fiy tfie staff;

4

Operating orders do not conflict with Technical Specification

requirements;

Incident reports detail no violation of Technical Specification

LCO or reporting requirements; and, -

Logs and records were maintained in accordance with Technical

Specifications and the procedures in 3.a above.

c.

__ T_he review included examination of the following plant shift logs

and operating records and discussions with licensee personnel:

Log No.

- Control Room Daily Log, August 4 - September 14, 1981

Log No.- 6 - Primary Pl ant Log, August 4 - September 14, 1981

Log No. 7 - Secondary Plant Log, August 4 - September 14, 1981

Log No. 8 - Unavailable Equipment Status Log, August 4 - September

14, 1981

Night Orders, August 4, 1981 - September 14, 1981

Lifted Lead and Jumper Log - All active

Tagging Requests - All active

Nonconformance Reports for July 1981

d.

In reviewing control room logs, the inspector noted that the control

room narrative log in both units had recorded overhead annunciator D-40,

Rod Deviation and Sequence, as inoperable for some time. Technical

Specification 4.1 .3.2.l states,

11 *** when the Rod Position Deviation Monitor

is inoperable, ... compare the demand position indication system and the

rod position indication system at least once per four hours.

11

Review of

the console reading sheets indicated that this special surveillance was

being accomplished by recording rod position every four hours, instead

of every eight as is the routine.

However, the inspector identified

several instances during one week period of review in which an interval

of eight hours had elapsed without recording rod position. During this

period, the alarm was inoperable as indicated by the narrative log.

The

following failures to conduct this surveillance were identified and the

time frame exceeded~the 25% extension allowed:

Unit l

Unit l

Unit 2

Unit 2

September 10, 1981

September 2, 1981

August 29, 1981

September l, 1981

0800 to 1600

1600 to 2400

1600 to 2400

0800 to 1600

  • 5

The above failures constitute apparent noncompliance with a Technical

Specification surveillance requirement (272/81-23-01) (311/81-21-01).

The inspector had no further questions relative to logs reviewed.during

this inspection period.

4.

Pl ant Tour

a.

b.

During the course of the inspection, the inspector made observations

and

(1)

(2)

(3)

(4)

(5)

(6)

(7)

(8)

(9)

(10)

( 11)

( 12)

( 13)

The

conducted multiple tours of plant areas, including the following:

Control Room (daily)

Relay Rooms

Auxiliary Building

'.Vital Switchgear Rooms

Turbine Building

Yard Areas

Radwaste Building

Penetration Areas

Control Point

Site Perimeter

Fuel Handling Building

Containment

Guard House

following determinations were made:

Monitoring instrumentation: The inspector verified that selected

instruments were functional and demonstrated parameters within

Technical Specification limits.

Valve positions. The inspector verified that selected valves were

in the position or condition required by Technical Specifications

for the applicable plant mode.

This verification included exam-

ination of control board indication and field observation of valve

positions (Charging/Safety Injection, Auxiliary Feedwater, and

Containment Spray Systems).

6

Radiation Controls. The inspector verified by observation that

control point procedures and posting requirements were being

followed.

Plant housekeeping conditions. The inspector observed that house-

keeping was generally acceptable.

Any cluttered or littered area~'*

for which maintenance was not in progress, was brought to the

attention of the plant management or operating staff.

Fluid leaks.

No fluid leaks were observed which had not been

identified by station personnel and for which corrective action

had not been initiated, as necessary.

Piping vibration.

No excessive piping vibrations were observed

and no adverse conditions were noted.

Selected pipe hangers and seismic restraints were observed and

no adverse conditions were noted.

Equipment tagging. The inspector selected plant components for

which valid tagging requests were in effect and verified that the

tags were in place and the equipment in the condition specified.

By frequent observation through the inspection, the inspector

verified that control room manning requirements of 10 CFR 50.54

(kl and the Technical Specifications were being met.

In addition,

the inspector observed shift turnovers to verify that continuity

of system status was maintained. The inspector periodically

questioned shift personnel relative to plant conditions and their

knowledge of emergency procedures.

Releases.

On a sampling basis, the inspector verified that appro-

priate documentation, sampling, autnorization, and monitoring

instrumentation were provided for effluent releases.

Fire protection. The inspector verified that selected fire exting-

uishers were accessible and inspected on schedule, that fire alarm

stations were inspected on schedule, that fire alann stations were

unobstructed and that cardox systems were operable.

Technical Specifications. Through log review and direct observa-

tions during tours, the inspector verified compliance with Technical

Specifications including Limiting_ ~q_n~tt\\lor}~ _f9r_Jlp~r~J.ion_ (LCO ~s) ._

i~~e r

0 ! ~~wi~~p~~~~~~~~r~o~~~~ n~!~~;~~~p!~~-i~~~~,l~~~~*~~~~c tfii~ l p~~~:r

shutdown margin, offsite power.

In addition, the inspector conducted

periodic visual checks of protective instrumentation and inspection

of electrical switchboards to confirm availability of safeguards

equipment.

7

Security. During the course of these inspections, observations

relative to protected and vital area security were made, in-

cluding access controls, boundary integrity, search, escort,

and badging.

d.

The following acceptance criteria were used for the above items:

Technical Specifications

Operation Directives Manual

Inspector Judgement

e.

The inspector had no further questions relative to tours made during

this inspection.

5.

Review of Periodic and Special Reports

upon receipt, periodic and special reports submitted by the licensee

pursuant to Technical Specifications 6.9.1 and 6.9.2 were reviewed by

the inspector.

This review included the following considerations:

The report included the information required to be reported by

NRC requirements;

Test resu'lts and/or supporting information were consistent with

design predictions and performance specifications;

Planned corrective action was adequate for resolution of identified

problems; and,

Determination whether any information in the report should be

classified as an abnormal occurrence.

Within the scope of the above, the following periodic reports were reviewed

by the inspector:

Unit 1 Monthly Operating Report - July 1981

Unit 2 Monthly Operating Report - July 1981

No unacceptable conditions were identified *

8

6. Licensee Events

a.

In Office Review of Licensee Event Reports

The inspector reviewed LERs submitted to the NRC:RI office to verify

that details of the event were clearly reported, including the accuracy

of the description of cause and adequacy of corrective action. The

inspector determined whether further information was required from the

licensee, whether generic implications were involved, and whether the

event warranted onsite followup.

The following LERs were reviewed:

UNIT 1

81-37/03L

81-38/03L

  • --

81-39/0lT

81-40/03L

  • --

81-41/03L

81-42/03L

  • --

81-43/03L

81-44/03L

81-45/03L

81-46/03L

  • --

81-4J/03L

  • --

81-48/03L

  • --

81-49/03L

81-50

81-51/03L

  • --

81-52/03L

RHR Pump Seal Failure

Loss of Audible Fire Alarm

Service Water Leak in Containment - No. 13 CFCU

Missed Surveillance

Reactor Coolant System Leakage - 1 PS 8

Reactor Trip System Instrumentation - No. 11 Pressurizer

Level Channel 3 Inoperable

Containment Air Lock 100

1 Elevation Outer Door Inoperable

Reactor Trip System Train B Inoperable During Surveillance

Test

Source Range Channel - N-31 - Inoperable

13 Containment Fan Coil Unit - Inoperable

Containment Air Lock 100 1 Elevation Outer Door Inoperable

Containment Air Lock 100 1 Elevation Outer Door Inoperable

Containment Air Lock (Elevation 100) - Cam Roller Inoperable

Not Used

Impingement of One Dead Shortnose Sturgeon, Acipenser

12A Intake Tras~ Bars

Engineered Safety Feature Actuation System Instrumentation

18 SEC Malfunction

UNIT 1

  • --

81-53/03L

  • --

81-54/0lT

  • --

81-55/03L

81-56/03L

  • --

81-57 /03L

81-58/04L

  • --

81-59/0lT

  • --

81-60/99XO

81-61/03L

  • --

81-62/03L

81-63/03L

  • --

81-64/0lT

81-65/03L

81-66/03L

81-67/03L

81-68/03L

UNIT 2

81-06/03L

81-07/03L

81-08

81-09/03L

e

9

lB Diesel - Inoperable - Water Jacket Leak

Volume Control Tank Level Control System

Loss of #12 & 22 Station Power Transformers

Reactor Coolant System - Leakage Detection System Failure

due to Loss of IF and lG Buses

Containment Air Lock 100

1 Elevation Outer Door Inoperable

due to Misalignment

Failure to Submit 1980 Radiological Report on Time

Check Valves 11MS46 and 13MS46 - Inoperable

Fire Suppression Water System - No. 2 Diesel Fire

Suppression Pump Inoperable

Pressurizer Over Protection System - Channel 1 Inoperable

Residual Heat Removal System Valving Misalignments

Individual Rod Position Indicators - 201 and 205 -

Inoperable

No. 15 Containment Fan Coil Unit - Service Water Leak

No. 15 Containment Fan Coil Unit (CFCU_t - Inoperable due

to Failed Flow Transmitter

No. 13 Containment Fan Coil Unit (CFCU} - Inoperable due

to Failed Flow Transmitter

No. 13 Containment Fan Coil Unit (CFCU} - Inoperable due

to Failed Flow Control Valve

Fuel Handling Building Fire Alarm Zone - Inoperable

Pressurizer Overpressure Protection System (POPS}

Inoperable

Failure of No. 22 Auxiliary Feedwater Pump to Start

Not Used

Boron Injection Tank - Out of Specification

UNIT 2

81-10/03L

  • --

81-ll/03L

  • --

81-12/03L

81-13/03L

  • --

81-14/0lT

81-15

  • --

81-16/03L

  • _...;.

81~17/03L

  • --

81-18/03L

81-19/03L

81-20

81-21/03L

  • --

81-22/03L

  • --

81-23/0lT

81-24

81-25

81-26/03L

81-27/03L

  • --

81-28/03L

81-29/03L

  • --

81-30/03L

81-31/03L

81-32/03L

81-33

10

Loss of Service Water Loop (21)

Containment Air Lock 100' Elevation Outer Door Inoperable

Containment Air Lock 130' Elevation Inner Door Inoperable

Containment Type B and C leak Rate Test Results Exceeded

Technical Specifications

Incorrect Cable Routing (Fire Protection)

Not Used

2B and 2C Diesel Generators Inoperable in Mode 5

Pressurizer Overpressure Protection (POPS) - Valve

Leakage

Overpressure Protection System - Channel 2 Activation

Rod 1B4 Position Indication System - Indicator Failure

Not Used

Auxiliary Feedwater Storage Tank (AFWST) Low Level

Movable Control Assemblies - Rod 2DLI, Dropped

Main Steam Isolation Valves - Closure Time Failure

Not Used

Not Used

2C Diesel Generator Overcurrent Trip

Valve 2PR6 Open/Closed Indication Malfunction

Onsite Power Distribution Systems - Trip of 2B40'.1 Breaker

Reactor Coolant Pump Flow Channel 2 Inoperable - Loop 22

No. 21 Auxiliary Feedwater Pump - Inoperable

Reactor Coolant System - Leakage Detection System Inoperable

Boron Injection Tank - Out of Specification

Not Used

,-------

UNIT 2

  • --

81-34/03L

  • --

81-35/0lT

81-36/03L

81-37/03L

81-38/0lT

  • --

81-39/03L

  • --

81-40/03L

81-41/03L

  • --

81-42/03L

  • --

81-43/03L

81-44/04T

  • --

81-45/9_9){

... -

81-46/03L

81-41 /03L

8l-48/03L

81-49/03L

  • --

81-50/03L

81-51/03L

81-52/03L

  • --

81-53/03L

11

Boric Acid Storage Tank - Out of Specification

Check Valves 21MS46 and 23MS46 - Inoperable

Pressurizer Pressure Channel I - Inoperable

Radiation Monitoring System - Containment Particulate

Channel - 2R11A - Inoperable

Service Water Leakage in Containment - No. 21 CFCU

Missed Surveillance - Channel Check of Post Accident

Monitoring Instrumentation (SP(0)4.3.3.7)

Chemical and Volume Control System Letdown Line Weld

Failure

Residual Heat Removal Suction Relief Valve Actuation and

Failure to Fully Reset

Reactor Coolant Temperature Less Than Minimum Required

For Power Operation

Overpressure Protection System Inoperable Due to Valve

Leakage

Inadvertent Contamination of On-Site Storage Area

Inadvertent Safety Injection During Unit Cooldown

Individual Rod Position Indication - 1B4 - Inoperable

Individual Rod Position Indication - 1SB2 - Inoperable

Individual Rod Position Indication - 2SA2 - Inoperable

Individual Rod Position Indications - 1SB4, 2SB2, and

2SB4 - Inoperable

2B Diesel Generator Start Time Failures

Boron Injection Tank - Out of Specification

Process Monitors 2Rl1A and 2R12A - Inoperable

Missed Surveillance - Containment Airlock

' ;

b.

Onsite Licensee Event Followup

(1) For those LERs selected for onsite followup (denoted by asterisks

in detail paragraph 6a), the inspector verified the reporting require-

ments of Technical Specifications and Regulatory Guide 1.16 had been

met, that appropriate corrective action had been taken, that the event

was reviewed by the licensee as required by AP-4, 6, and 7, and that

continued operation of the facility was conducted in accordan~e with

Technical Specification limits. The following findings~**reM.te to the

LERs reviewed on site:

Unit 1

81-39/0lT

--

81-64/01 T

--

81-41/03L

81-43/03L

81-47/03L

81-48/03L

81-49/03L

81-57 /03L

--

81-52/03L

--

81-53/03L

These containment service water leaks resulted from

failure of a dissimilar metal weld.

As noted in LER

50-272/81-64/0lT, a design change is nearly completed

which makes piping modifications to remove dissimilar

metal welds.

The change is completed on No. 13 CFCU.

This report documents unidentified reactor coolant

system leakage in excess of 1 gpm.

Investigation iden-

tified the leakage source to be packing on instrument

valve 1 PS 8.

Having identified the source as a packing

leak the applicable limit was 10 gpm and the observed

leakage rate of 2.69 was acceptable. The packing was

subsequently replaced.

The licensee has concluded that air lock failures are

attributable to improper operation.

As already docu-

mented, a program to strengthen air lock door components

has been completed.

In addition, annual requalification

training for all station personnel who may have occasion

  • to use a containment airlock includes specific guidance

for careful operation of the doors. This area will be

the subject of continuing review to ensure that licensee

actions are effective in improving air lock reliability.

This event is discussed in NRC Inspection Report 50-272/

81-12, detail 13.b. Licensee actions to correct SEC

voltage sensitivity will be followed as unresolved item

81-12-07.

This report details failure of a diesel jacket water

piping nipple due to improper use of the piping as

support by an individual. The report does not address

corrective action for the apparent cause identified.

Tfte licensee stated that a supplemental report will be

submitted when effective corrective action is identified *

This item is unresolved (272/81-23-02).

--

81::.::54/01 T

--

81-55/03L

--

81-59/01 T

--

81-60/99){

--

81-62/03L


~---------

l

13

This report details a potential for damage to centri-

fugal charging pumps under a postulated failure of

the VCT level control system.

Such failure has been

identified by Westinghouse as not meeting the require-

ments of GDC-24 and IEEE-279.

The licensee has taken

action to ensure that operators are aware of this type

of failure and are alerted to other instrumentation

available to confinn VCT level. The inspector had no

questions relative to action taken by the licensee to

preclude failure of the centrifugal pumps.

However,

the question of compliance with regulatory requirements

relative to instrumentation and control design is un-

resolved pending further review (272/81-23-03).

This event is discussed in NRC Inspection Report 50-

272/81-12. The inspector confirmed that licensee

preventive measures have been taken to preclude testing

of the Unit 3 breaker in a condition which would jeopar-

dize the 13 KV ring bus. These measures included a

caution tag on the breaker and modification of Operating

Memo-5 which relates to operation and testing of the

Unit 3 output breaker. The inspector had no questions

with respect to interim measures taken, noting that

DCR 1 SC-0577 has been initiated to precipitate a

permanent design solution.

This event is detailed in NRC Inspection Report 50-272/

81-14.

The licensee is conducting monthly radiography

to confinn the integrity of the check valve internals

while seeking a permanent solution to the apparantly

high wear rate on the valves. This item is unresolved

pending completion of the licensee's analysis and sub-

mittal of a supplementary report (272/81-23-04).

No. 2 Fire Pump failed to start during a surveillance

test due to failure of the diesel engine.

The engine

was sent to the vendor for repair and overhaul, and

was returned to service in late August.

As committed

in the LER, the licensee will submit a supplemental

report detailing the nature of the failure. This i tern

is unresolved (272/81-23-051.

Following inspection of No. 11 RHR Pump and Heat Ex-

changer for loose camera parts on June 20, 1981 (refer-

ence NRC Inspection Report 50-272/81-14} the system

was aligned for return to service and an ASME Section

XI pump test performed at approximately 8:45 p.m.

\\

14

8l-62/03L

The results of the test were acceptable but, when re-

(continued)

viewed later, appeared to have resulted in lower than

expected differential pressure. At 1:48 a.m. on June

21, -the unit was heated from Mode 4 to Mode 3 and went

critical at 9:45 a.m.

At noon on June 21, the pump

test was repeated to resolve the question of low dif-

ferential pressure and at that time the heat exchanger

inlet valve, 11 RH 14, was found closed. With this

valve in the closed position, the No. 11 train of

Unit 2

81-ll/03L

--

81-12/03L

--

81-14/0lT

--

81-16/03L

_,,,_

81-JJ /03L

81-43/03L

RHR was rendered inoperable. The valve was immediately

opened and a satisfactory pump test conducted.

The

LER notes that the verification valve lineup required '

by procedure had not been conducted.

The inspector

further noted that mode changes with less than the

required available ECCS subsystems are prohibited by

Technical Specification 3.0.4. This event contributes

to an apparent item of noncompliance (272/81-23-06).

These reports detail failures of Unit 2 airlocks.

Corrective action described for Unit l LER 81-43/03L

above involves station-wide training and should be

effective in reducing the number of failures in both

units.

This event is discussed in NRC Inspection Report 50-

311/81-11. Correct cable routing was verified by the

inspector shortly after tne error was discovered and

corrected.

A stuck: relay in the diesel generator field flash

circuitry resulted in two inoperable diesels while in

Mode 5.

Tne inspector noted tnat there appeared to be

no periodic surveillance of relays to preclude this

type of occurrence.

Tfie licensee stated that a program

of relay cleaning will be initiated. This item is

unresolved (311/81-21-021..

These reports detail inoperability of the Pressurizer

Overpressure Protection (POPS) system while below 312°F

due to leakage through valve 2 PR 2 or 2 PR 47.

Despite

repairs during the most recent cooldown, the POPS and/or

PORV continued to leak and have 5een isolated. The

licensee establishes the vent path required by Technical

Specifications within the time limits stated.

LER 81-

43 states that repairs will be made during the next re-

fueling outage. Supplements to both LER

1s will be

submitted following repair. This item is uriresol_ved

pending va_lve _r!=!pair and receipt.,,and)re;vJew of'* the sup-

p 1Ein:iental reports" ( 3ll /81-23-03}:

  • .

. . .

15

81-18/03L

This inadvertent actuation of the POPS system was

caused by miscommunication between an instrument

foreman and the shift operators. Based on review

of procedures and discussions with personnel, the

inspector detennined that adequate controls to prevent

recurrence were in place.

81-22/03L

This event is discussed in NRC Inspection Report 50-

311/81-11. The inspector had no further questions.

81-23/0lT

Testing of main steam isolation valves revealed that

under the condition of a hydraulic opening in progress,

rapid shutting of the valves could not be accomplished

in less than 5 seconds as required by Technical Speci-

fications. Design changes were made in both units to

ensure that closure under isolation conditions could be

accomplished within the required time under all circum-

stances.

81-28/03L

During a safeguards loading sequence (Safety Injection

on June 3, 19811, starting of the second CFCU on the

B vital bus caused the 2B4D feeder breaker to tr1p.

It was later determined tnat a relay modification, al-

ready installed on Unit 1, to raise the overcurrent

setting had not been made on Unit 2. The modification

was subsequently made to the 2B and 2C bus feeder

oreakers. Failure to detect this problem earlier can

also be attributed to a prior practice of testing the

accident load"ing sequence witfiout all equipment avail-

aole. Remaining equipment was tested later as it was

returned to service. As a result, the breaker over-

current setting may not fiave oeen challenged prior to

this event. The licensee stated that such testing

practices will 5e prohibited during future surveillance

testing of this type. The inspector had no further

questions on tfiis item.

81-30/03L

Th-is event is detailed in NRC Inspection Reports 50-311/

81-11 and 81-13.

81-34/03L

During a re-fill of the Boron Injection Tank (BIT)

following safety injection, failure to completely drain

tfie Bii resulted in dilution of the Boric Acid Storage

Tank (BASTI to less than 20,000 ppm.

The procedure did

not include a method for verifying the BIT completely

drained prior to placing it on recirculation with the

_BAST.

The inspector reviewed Revision 1 to OI II-4!3,05,

Flastiing, Draining, and Filling the Boron Injection Tank,

approved oy SORC on August 31, 1981. The procedure now

calls for use of a local sample point (ISJ6) to confinn

that the BIT is empty.

The inspector had no further

questions.

16

--

81-35/0lT Corrective action for this item is similar to that

described for Unit 1 LER 81-59/0lT above and will be

evaluated concurrently.

--

81-39/03L Technical Specification 4.3.3.7 requires a monthly

channel check of post-accident monitoring instrumen-

tation. The licensee had prepared a surveillance

procedure to accomplish this activity but had not

scheduled the test in the Inspection Order system. *

As a result, the test conducted on April 22, 1981

became overdue on May 30, 1981.

The oversight was

discovered on June 6, 1981 and reported as a missed

surveillance in this LER.

During the period June 2-4,

1981, several plant startups from Mode 3 to Mode 1

were conducted.

In accordance with Technical Speci-

fication 4.0.3, failure to conduct required surveillance

constitutes inoperaoility of the applicable component.

As a result, tnesemode changes contribute to apparent

noncompliance with Technical Specification 3.0.4

(311/81-21-04}.

--

81-40/03L The failed CVCS vent line was capped.

Not stated in

the report, but confirmed by the inspector, was the

nondestructive examination of several similar config-

urations in tne system.

No other prob*1 ems were identi-

fied.

--

81-42/03L During heavy feeding of steam generators at approximately

6 percent power, Tave decreased below the minimum for

criticality (541oFl.

The excursion lasted for 13 minutes,

less than the 15 minutes permitted by the Technical

Specification Action s*tatement.

The inspector confirmed

oy ooservation during several startups that operators

remain acutely aware of temperature 1 imits and take

prompt action to maintain $pecifi ed parameters.

--

81-45/99X This safety injection was caused by failure to closely

monitor steam generator differential pressures during

a cooldown.

Tne inspector confirmed that procedures for

cooldown using atmospheric relief valves (MS 10) caution

tne operator to maintain differential pressures less than

JOO psid.

In ooserving cool downs, the inspector has

ooserved tfiat differential pressure information is readily

avalla6le and dlligently monitored-';. by operators. The

inspector had no further questions.

--

81-50/03L

--

81-53/03L

17

This report details a series of failures of 28 Diesel

Generator to start within the 10 seconds required by

Technical Specifications. Fol lowi.ng arnumber of other

repairs, it was determined that one of the turbo-boost

air supply solenoids had failed and its redundant

counterpart was wired incorrectly. A subsequent check

of all diesel solenoids has been conducted and no

wiring errors discovered.

The licensee is reviewing

all diesel failures to start and will submit a supple-

mental report. This item is unresolved (311/81-21-05).

Technical Specification 4.6.1.3.b requires a containment

air lock pressure test prior to establishing containment

integrity if it has 6een broken. This requirement had

not been incorporated into procedures for Unit 2 and

does not exist for Unit 1. On June 21-22, 1981 the unit

changed from Mode 5 to Mode 1 following a maintenance

outage during wni'di containment work required that con-

tainment integrity oe 6rol<en.

The air lock test was

not conducted prior to mode change.

When the omission

was discovered on July 1, 1981 a successful test was

conducted. Failure to demonstrate operaoility of the

air lock in accordance with the schedule specified in

Technical Specifications contributes to apparent non-

compliance with Technical Specification 3.0.4 (311/81-

21-041.

c. Tfie following Unit 1 LERs, reviewed above, were submitted later than the

ti!ne required 5y Technical Specifications; 81-40/03L, 81-45/03L, and

81-52/03L. Late reporting was tne saoject of an item of noncompliance

identified in NRC Region I correspondence to the licensee dated June 24,

1981.

Tne events listed aoove occurred prior to July 15, 1981, the date

oy wFLidi tfie 1 icensee committed to nave corrective action in pl ace to

preclude late reporting. Effectiveness of licensee actions in this regard

will be evaluated during a subsequent inspection.

Tfie inspector had no further questions with respect to LERs reviewed.

J. * Tull *Power * L itense *Condi tfons (Un it* 2}

On January14, 1981, April 28, 1981, and May19, 1981, the NRC staff, in-

cluding the Senior Resident Inspector, 5riefed the Commission on the status

of Salem Unit 2 and the proposed licensing action to authorizec:'operation in

excess of 5 percent rated thermal power.

The full power license for Salem

.Unit 2 was issued on May 20, 1981 and contains several conditions to be met

prior to given dates or events. Tfle inspector reviewed a number of these

items to determine status of implementation.

The following comments apply

to tne areas *revi"ewed (Numbers refer to paragraph references in the full

power 1 icense)_:

18

2.C.(lO)(d), (f), and (h) Fire barrier and cable wrap program.

The licensee has stated that this program is complete. A special

NRC inspec.tion has been scheduled to confirm the engineering

analysis and field installation of fire barriers. During this

inspection period, a sampling of items, to be completed by July

31, 1981, in accordance with paragraph (d), was inspected. Based

on walkthrough inspections, the additional cable wrap, barrier

extensions and smoke detectors appear to be in place.

One excep-

tion was ooserved. Paragraph 2.C.(10)(9) requires the licensee

to wrap one of the redundant power cables from the diesel generators

located in the fuel oil storage tank room.

Neither of the redundant

feeds llad 15een wrapped when ooserved on September 1, 1981.

When

identified to the licensee, a fire watch was immediately established

and work initiated to wrap the B diesel power cable. Subsequent

licensee review of the design change package indicated that the work

had not oeen accomplished as directed. A review of the package by

tne licensee indicated that all other work called for by the design

cfiange llad oeen completed. Failure to wrap the diesel power cable

constitutes apparent noncompliance with a condition of facility

operating license DPR-75 (311/81-21-06).

Complete confirmation of

tfiis license condition will Be included in a subsequent inspection.

2.C.(l2lCompletion of Preoperational Testing of Circulating Water

System. Startup Procedure 34, Circulating Water System and Sodium

_Bypocfil orfte System was completed on July 24, 1981, with the excep-

tion of a data set on Circulator 228 wnile operating (taken on July

27, 1981[ and completely automatic operatfon of the sodium hypo-

clll orite system due to incompatioility of installed equipment with

current EPA standards (operating 111ainly under operator control).

Operatfon of tile Circulating Water System was verified as proper

prfor to power ascensfon aoove 50 percent. The inspector reviewed

tile completed startup procedure and discussed the test with cognizant

engtneers*.

No items of noncompliance were identified.

2.C.(141 Waterhammer test. As discussed in NRC Inspection Report

50-311/81-1~ tfie feedwater hammer test was conducted on July 23, 1981

prior to operation a5ove 90 percent rated thermal power.

No unaccep-

ta51 e piping displacement was recorded.

2.C.(241(c1liil 48 Hour endurance run of Auxiliary Feedwater Pumps.

Tfie*motor driven pumps (No. 21 and 22) were tested on August 18, 1980.

Testing of tile steam-driven pump (No. 23) was completed on August 14,

1981. Tfie inspector reviewed test results which indicated acceptable

nearing temperatures and vioration readings for the pumps.

Testing

was completed prior to operation at 100 percent power as required

oy tfie license. The licenseers 60-day report will be reviewed when

received (311/81-21-07}.

Tfie inspector had no further questions with respect to license conditions

reviewed.

19

8. Operating Events

a. Unit 1

(ll At 2:38 p.m. on August 10, a reactor/turoine trip occurred due to

a low level in No. 12 Steam Generator fo 11 owing a loss of No. 11

Main Feed Pump. Maintenance department investigation was unable

to identify any pro5lem witfi tfie pump. First out indication was

not availa5Je due to a 5lown fuse on tfie feed pump indicator panel.

Power operation resumed at 4:25 a.in. on August 11 with No. 12

"Main Feed Pump.

No. 11 Feed Pump was run for several hours to

monitor its operation and was returned to service with no apparent

prolilems.

J:i *.. Unit 2

(1L At 4:15 a.-m. on August 10, Salem Unit 2 was shut down (Mode 3) to

repat.r pacR.ing leaks on two valves in the Reactor Coolant System

11RTD

11 .oypass line. Tfie total leal<.age was 11.5 GPM as measured by

an RCS inventory oalance.

Power operation resumed at 4:25 a.m.

on August 11.

(21 The plant tripped from 100 percent power at 8:40 p.m. on August 22,

.due to low-low level in No. 24 Steam Generator caused oy loss of

No. 22 Steam Generator feedwater pump.

Tne pump tripped on indicated

low suctfon pressure attriouted to secondary plant fluctuations or speed

control oscillation. following system trou6leshooting, the unit re-

srn:ned power operation at 10:35 a.in. on August 23.

DL A *moisture carryover test using a NA-24 tracer at 100 percent power

was conducted on August 29. At 10:45 a.m. on August 29, power was

reduced to 25 percent 5ecause of steam generator cation conductivity,

res.al ting from a condenser tuoe l eaK..

Bl owdown was initiated at

1:11 p.-in. on August 29*, to restore steam generator cfiemistry. Blow-

down to tfie non-radwaste 5asin witn known quantities of radioactive

fsotope in tlie steam generator was treated as a liquid release with

tne Jilowdown radiation monitors serving as the rel ease monitors.

Estimated activity released over the period was 0.5Ci, and is con-

ststent witfi Tecfinfcal Specification Appendix B limits *

.. GI On August 31, steam generator chemistry and activity levels were

reduced suffi.ciently to support increase in power.

At 4:41 a.m. on

August 31, No. 22 Steam Generator Feed Pump (SGFP) tripped on

indicated overspeed witfi tfie plant at 85 percent power.

The resulting

transient caused a tur5ine trip/reactor trip on high level in No. 21

Steam Generator at 4:47 a.m. Trouolesfiooting was perfonned on No.

22 SGFP controls and power operations resumed at 6:24 p.m.

20

(5)

The 100 percent generator trip test was conducted at 9:24 a.m.

on September 2, followed by the last natural circulation test,

boron mixing and cooldown. * All systems functioned normally on

the trip with no safety injection initiated. The unit returned

to power operation at 7:19 a.m. on September 3.

(6) At 4:10 p.m. on September 3, and following a review of the cali-

bration data (Startup Tests) for both channels of steam flow

indication for No. 21 steam generator, the licensee declared the

instruments inoperable and shutdown the unit. The square root

of the steam flow dp was non-linear above 92 percent power, with

moisture carryover considered to be the cause. The instruments

were recalibrated for their linear response range (below 92 per-

cent). Power operations resumed at 7:45 a.m. on September 4.

The licensee has imposed an operating limit of 90 percent power

pending an evaluation and resolution of the non-linear steam flow

indications and high moisture carryover experienced by No. 21

steam generator above 92 percent.

l7) At 7:40 p.m. on September 11, the licensee conducted a second

steam generator moisture carryover test at 100 percent power

using NA-24 tracer. Operation above 90 percent during this test

caused both channels for No. 21 steam generator steam flow in-

dications to trip their respective bistables.

The results are being evaluated by the licensee and the NSSS

vendor.

Preliminary review of the data confirm the results of

the first carryover test. At 9:50 a.m. on September 12, the test

was complete, and power was reduced to 25 percent because of high

cation concentration in the steam generators.

At 10:49 p.m. on September 13, reactor power was returned to 90

percent when the blowdown system was returned to service in order

to reduce the cation concentration in the steam generators.

The inspector had no further questions relative to operating events listed

above or the licensee's corrective action.

9.

Surveillance Activities

The inspector observed licensee's performance of the following surveillance

procedures:

a.

PD 18.1.001 Solid State Protective System - Periodic Test

b.

SP(O) 4.0.5 P - Auxiliary Feedwater System - pumps 21 and 23

c. SP(nl 4.0.5 V - Auxiliary Feedwater System - valves (partial)

(No. 2MS132)

21

The inspector confirmed that testing was performed in accordance with

adequate procedures, test instrumentation was calibrated, limiting

conditions for operations were met, removal and restoration of the

affected components were properly accomplished, and test results conform

with Technical Specifications and procedure requirement and were reviewed

by personne*1 otfler tflan the indiv'fdual directing the test. Any deficiencies

noted were reviewed and resolved by the personnel of the responsible de-

partment. The personnel performing the surveillance activities were

knowledgeable of the system and the test procedures. The inspector con-

cluded that they were qualified to perform the tests and had no further

questions regarding the performance of these surveillance activities.

10. System Operation and Review

The inspector conducted a walk down of the accessible portion of the

Auxiliary Feedwater System of Unit 2. Licensee's drawing 205336, No. 2

Unit Auxiliary Feedwater Piping Diagram, revision 6, dated April 11, 1980,

was used for this walk down.

The inspector found no unexpected conditions

with the exceptions of a two inch pipe which had been welded between the

drain line on the discharge piping of No. 23 Auxiliary Feedwater Pump and

the drain line of the corrnnon suction header from the Auxiliary Feedwater

Storage Tank.

This pipe had been installed by design change, 2 ET-0760,

to support a 48 hour5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> test run of the No. 23 Auxiliary Feed Pump which was

performed as part of the Startup Test Program.

The drawing in use by the

inspector had been appropriately marked,

11DCP ISSUED.

11

When the Operational

Design Change Status Notice Report, dated August 1, 1981, was reviewed,

several design change packages were indicated as affecting this drawing,

but the change package installing tfle two inch pipe and the current status

was not indicated on the status report. This item is unresolved pending

further review (311/81-21-08).

11.

Fuel Receipt

The licensee received 56 new fuel assemblies which are scheduled for in-

stallation during unit 1 refueling outage later this year. The fuel

assemblies were removed from their shipping casks, inspected, and placed

in the new fuel storage racks (dry). The inspector witnessed unloading,

transfer, and storage of 10 assemblies. The inspector confirmed that

acceptable procedures were approved and were in use. The licensee stated

that no unacceptable conditions were identified in any of the 58 fuel

assemblies.

The inspector reviewed the shipping documents and receipt

inspection documents. Daily checks of the cranes had been performed, and

weekly checks of the overload cutout had been performed within seven days

of fuel movement.

The inspector noted no unsatisfactory conditions and

had no furtfler questions regarding the receipt of new fuel.

22

12. Startup Testing

13.

14.

The inspector observed portions of startup testing conducted during this

period. Observations included the following; correct procedure in use,

crew requirements, test prerequisites, plant conditions, calibrated test

equipment, adherence to procedure, coordination, data collection, and

preliminary data review.

Portions of the following tests were observed:

SUP 82.1 - Load Swing Tests

SUP 82.2 - Large Load Reduction Tests

SUP 82.8 - NSSS Acceptance Test

SUP 82.9 - Generator Trip from 100 percent Power

Comments relative to observations of the above Startup Test are provided

in a separate NRC Inspection Report 50-311/81-22.

Operator License Examination

On September 4, 1981, the Senior Resident Inspector administered a written

partial re-examination to two applicants. The inspector was present for

the entire examination and identified no unacceptable conditions or practices.

Unresolved Items

Areas for which more information is required to determine acceptability are

considered unresolved. Unresolved items are contained in Paragraphs 3, 6,

7 and 10.

15. Exit Interview

At periodic intervals during the course of this inspection, meetings were

held with senior facility management to discuss inspection scope and

findings.