ML18010A619

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Insp Rept 50-400/92-04 on 920215-0320.Violations Noted. Major Areas Inspected:Plant Operations,Radiological Controls,Security,Fire Protection,Surveillance,Maint & Spent Fuel Handling Activities
ML18010A619
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 04/10/1992
From: Christensen H, Shannon M, Tedrow J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18010A617 List:
References
50-400-92-04, 50-400-92-4, NUDOCS 9205050111
Download: ML18010A619 (25)


See also: IR 05000400/1992004

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W.

ATLANTA,GEORGIA 30323

Report No.:

50-400/92-04

Licensee:

Carolina

Power

and Light Company

P. 0.

Box 1551

Raleigh,

NC 27602

Docket No.:

50-400

Facility Name:

Harris

1

Inspection

Conducted:

February

15 - March 20,

1992

Inspectors:

edrow, Senior

esi ent

nspector

n

.

Shannon

Resident

Inspector

Approved by:

H. Christensen,

Section Chief

Division of Reactor Projects

License

No.:

NPF-63

't lo eW

a

e

igne

la

Date Signed

g /u y~.

ate Signed

Scope:

SUMMARY

This routine inspection

was

conducted

by two resident

inspectors

in the areas

of plant

operations,

radiological

controls,

security,

fire protection,

surveillance

observation,

maintenance

observation,

safety

system

walkdown,

review of

PNSC activities,

review of spent

fuel handling activities,

design

changes

and modifications

and

review of licensee

event reports.

Numerous

facility tours

were conducted

and facility operations

observed.

Some of these

tours

and observations

were conducted

on backshifts.

Results:

,t

Two violations

were identified:

Failure to properly identify and correct

deficiencies

as

requi red

by

10 CFR 50, Appendix B, Criterion XVI, paragraphs

2.a.(1)

and 9.b;

Failure to use

a qualified person for the

performance

of

independent verifications,

paragraph

3.a.

Housekeeping

improvement

was

needed

in several

plant areas,

paragraph

2.b.(3).

ALARA planning for the outage

work and Reactor

Coolant

Pump

(RCP) oil addition

was considered

to be

a strength,

paragraph

2.b.(4).

The

RAB area

radiation levels

have

increased

significantly due to Residual

Heat

Removal

(RHR) shutdown cooling operation,

paragraph 2.b.(4).

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Detailed planning

and

use of mockups for maintenance activities

was considered

to be

a strength,

paragraph

4.a.

Personnel

training regarding

the

use of freeze

plugs

was considered

thorough,

paragraph

4.c.

Licensee

management

has reevaluated

spent fuel crud cleanup efforts and decided

to leave the crud

on the bottom of the pools,

paragraph

7.

The conservative

decision to shutdown

the plant

and repair boric acid leakage

reflected

management's

support

for the control

of boric acid corrosion,

paragraph

8.

REPORT

DETAILS

Persons

Contacted

Licensee

Empl oyees

J. Collins, Manager,

Operations

  • C. Gibson,

Manager,

Programs

and Procedures

  • C. Hinnant,

General

Manager,

Harris Plant

  • B. Meyer, Manager,

Environmental

and Radiation Monitoring

T. Morton, Manager,

Maintenance

  • J. Hevill, Manager,

Technical

Support

C. Olexi k, Manager,

Regulatory Compliance

A. Powell, Manager, Harris Training Unit

R. Richey, Vice President,

Harris Nuclear Project

  • H. Smith, Manager,

Radwaste

Operation

E. Willett, Manager,

Outages

and Modifications

  • W. Wilson, Manager,

Spent Nuclear

Fuel

Other

licensee

employees

contacted

included

office,

operations,

engineering,

maintenance,

chemistry/radiation

and corporate

personnel.

  • Attended exit interview

NRC Personnel

  • D. Roberts,

Resident

Inspector,

Intern

Acronyms

and initialisms

used

throughout this report are listed in the

last paragraph.

Review of Plant Operations

(71707)

The plant

began this inspection

period in power operation

(Mode 1).

On

March

7

a power reduction

was

commenced

and oil was

added to the

A and

8

reactor

coolant

pumps.

The unit was then

taken off-line at 4: 18 a.m. to

perform repairs

to valve

1RC-22,

AD bypass manifold isolation valve (see

paragraph

8 for more details

on the plant outage).

The

271

days of

continuous

plant operation

on line set

a

new plant record.

Following

completion of valve repairs,

a plant heatup

was

commenced

and the plant

was

taken to hot standby

(Node 3) at 7:38 a.m.

on March 11.

A reactor

startup

was

performed

on March

12

and the reactor

was

taken critical at

12:20

p.m.

The plant

was returned

to power operation

at 7:24

p.m.

on

March

12 where it remained for the duration of this inspection period.

a.

Shift Logs

and Facility Records

The inspector

reviewed

records

and

discussed

various entries

with

operations

personnel

to verify compliance

with the

Technical

Specifications

(TS)

and the licensee's

administrative

procedures.

The following records

were reviewed:

Shift Supervisor's

Log; Control

Operator's

Log;

Outage

Shift Manager's

Log;

Night Order

Book;

Equipment

Inoperable

Record;

Active Clearance

Log;

Jumper

and Wire

Removal

Log; Temporary Modification Log; Chemistry Daily Reports;

Shift Turnover Checklist;

and selected

Radwaste

Logs.

In addition,

the inspector

independently verified clearance

order tagouts.

The inspectors

found the

logs to

be readable,

well organized,

and

generally provided sufficient information on plant status

and events.

Clearance

tagouts

were found to be properly implemented.

(I)

During control

room observations

on

February

20,

1992,

the

inspectors

noticed that the control

room

HVAC system

was aligned

for emergency

recirculation.

This situation

occurred

as

a

result

of

a control

room isolation

signal

from

a failed

radiation monitor.

The inspectors

noticed,

however, that alarms

were lit on

the control

board

indicating that

the required

positive pressure

in the control

room was not being maintained

by this system.

TS 4.7.6.d.3

requires

a 1/8 inch water gauge of

positive

pressure.

This matter

was

reported

to operating

personnel

who indicated that efforts were currently in progress

to investigate

the cause for the inadequate

positive pressure.

The following day the inspectors

were informed of the results of

the

investigation.

An

access

door

to

the

ventilation

recirculation

fan unit

R-2B

was

found partially

open

which

allowed

enough air leakage

from the unit to prevent

adequate

pressurization

of the control

room.

The inspectors

were further

informed that it was

a routine practice for auxiliary operators

to open

these

access

doors during rounds to check the condition

inside

the ventilation unit.

Apparently

the

door

was

not

properly closed following the last inspection.

The inspectors

determined

that

no control

room log entries

or

ACRs

had

been

generated.

Procedure

PLP-002,

Corrective

Action

Program,

section

5.2, requires

an

ACR or other sub-program

document

be

initiated for identified deficiencies.

The inspector considered

the

documentation

of

the

problem

to

be

inadequate

for

determining

appropriate

operability

and potential

corrective

actions.

Upon notification of this finding, licensee

personnel

initiated

an

ACR to document

the ventilation problem.

On March

2 the door for control

room ventilation unit R-2A was also found

to be inadequately

shut.

The door was resecured

and

a log entry

made in the shift foreman's

log.

In

NRC Inspection

Report 50-400/92-02,

the failure of operators

to properly identify deficiencies

for appropriate

corrective

action

was identified and

a non-cited violation

(NCV 400/92-02-

01)

was

issued.

The occurrence

of the inadequate

operation of

the control

room ventilation

system deficiency indicates

that

additional

licensee

management

attention is needed

in this area.

The fai lure to properly document

the deficiency in the control

Ci

room

emergency

ventilation

system

is

contrary

to

the

requirements

of

10 CFR 50,

Appendix

B, Criterion

XVI and is

considered

to be

a violation.

Violation (400/92-04-01):

Failure to properly identify and

correct

deficiencies

as

required

by

10 CFR 50,

Appendix

B,

Criterion XVI.

b.

Facility Tours

and Observations

Throughout

the inspection

period, facility tours

were conducted

to

observe

operations,

surveillance,

and

maintenance

activities

in

progress.

Some

of

these

observations

were

conducted

during

backshifts.

Also, during this inspection period,

licensee

meetings

were attended

by the inspectors

to observe

planning

and

management

activities.

The facility tours

and

observations

encompassed

the

following areas:

security perimeter fence;

control

room;

emergency

diesel

generator

building;

reactor

auxiliary building; reactor

containment

building; waste

processing

building; turbine building;

fuel

handling building;

emergency

service

water building; battery

rooms; electrical

switchgear

rooms;

and the technical

support center.

During these tours,

the following observations

were made:

( 1)

Monitoring Instrumentation

- Equipment operating

status,

area

atmospheric

and liquid radiation monitors, electrical

system

lineup,

reactor

operating

parameters,

and auxiliary equipment

operating

parameters

were

observed

to verify that indicated

parameters

were

in accordance

with the

TS for the current

operational

mode.

(2)

Shift Staffing - The inspectors

verified that operating shift

staffing was in accordance

with TS requirements

and that control

room

operations

were

being

conducted

in

an

orderly

and

professional

manner.

In addition,

the inspector

observed shift

turnovers

on various occasions

to verify the continuity of plant

status,

operational

problems,

and

other

pertinent

plant

information during these

turnovers.

(3)

Plant

Housekeeping

Conditions

-

Storage

of material

and

components,

and

cleanliness

conditions

of various

areas

throughout

the facility were

observed

to determine

whether

safety and/or fire hazards

existed.

The inspectors

found plant housekeeping

and

component material

condition to

be satisfactory.

However,

the inspectors

noted

that

cleanliness

in certain

plant

areas

had

deteriorated.

Specifically,

the charging/safety

injection

pumps

continuously

exhibit oil leakage

even after repeated

maintenance.

Two motor

operated

valves

(1CS-217

and

1CS-291)

also exhibited oil leakage

from the

valve actuator.

Fittings

on

two sodium hydroxide

addition tank level transmitters

(LT-1CT-7150A and LT-1CT-7166B)

also

showed

signs of leakage.

The containment

spray

pump

and

(4)

RHR

pump

rooms

have

ground water intrusion problems

and water

has

been

observed

to collect at

low points

on

the floor.

Although these

problems

were identified by licensee

personnel,

and

appropriate

work tickets

were written to correct

these

problems,

corrective maintenance

has not yet been performed.

Radiological

Protection

Program - Radiation protection control

activities

were

observed

routinely to verify that

these

activities

were in conformance

with the facility policies

and

procedures,

and in compliance with regulatory requirements.

The

inspectors

also

reviewed

selected

radiation

work permits

to

verify that controls were adequate.

The inspector

attended

the pre-job

ALARA briefing for the

A and

B reactor

coolant

pump motor oil addition job and reviewed the

RWP

and

previous

radiation

surveys

for the

areas

inside the

containment

building where the work was to be performed.

This

was

the

second

time

a containment

entry

had to be

made to add

oil to

a reactor coolant

pump.

Previously in October

1991,

an

entry was

made to add oil to the "B" reactor coolant

pump motor.

Again licensee

management

utilized mockup training

on

a spare

motor stored in the spare parts

warehouse.

Lessons

learned

from

the previous

entry were utilized to refine the techniques

for

the

current oil addition

plan.

These

efforts

were

very

successful

in limiting personnel

exposure

received

by plant

personnel.

P

During the forced

outage,

the

licensee

faced

a challenge

in

keeping radiation

exposure

to

a minimum while repairing valves

1RC-22

and

1RC-953.

These

valves

were located

near

the

"C"

reactor

coolant

loop where

the radiation

exposure

rates

were

high.

However,

through

a

combination

of effective pre-job

planning, optimization of worker stay-time,

and coordination of

work efforts

between different organizations,

the licensee

kept

exposure

levels to

a minimum.

The biggest contributor to the

reduced

exposure

levels

was the pre-job planning which included

the

use of lessons

learned

from a similar outage in May 1990.

The licensee

also

made

use of a videotape of the work area which

allowed

the licensee

to plan the job without having to make

repeated

entries

into the

hazardous

area.

This effective

use

of ALARA planning

was considered

a strength.

The plant

was

faced with another radiological

challenge

as

a

result of operations

during the outage.

Initially, the licensee

planned

to repair valves

1RC-22

and

1RC-953 while in Mode 5.

based

on this the licensee

planned

a chemical

cleaning

process

designed

to loosen corrosion

products

in the

RCS.

This process

would normally be followed by

a flushing process

(while in Node

5) to remove these

products

from the primary system.

During the

outage,

licensee

management

decided

that the valves

could

be

repaired while in Node 4.

Since the flushing could not occur in

Mode 4, the

RHR system

(while in shutdown cooling) retained

a

significant amount of the highly radioactive corrosion products.

As

a

result,

radioactivity

in

the

RHR

system

increased

significantly when corrosion

products settled

out in the system

following its return to a normal

standby status.

This condition

presents

a

new challenge

to the plant because

several

areas

of

the

RAB have

been

upgraded

to high radiation

areas.

The

licensee

took

steps

to conspicuously

identify/post affected

areas.

The licensee

has

no definite

plans

to

reduce

the

radioactivity in the

RHR system

before

the fall

1992 outage.

The

inspectors

will continue

to

monitor

the

licensee's

activities in this area.

(5)

Security Control -

The performance

of various shifts of the

security force was

observed

in the conduct of daily activities

which included:

protected

and vital

area

access

controls;

searching

of personnel,

packages,

and vehicles;

badge

issuance

and retrieval; escorting of visitors; patrols;

and compensatory

posts.

In addition,

the inspector

observed

the operational

status

of closed circuit television monitors,

the Intrusion

Detection

system

in the central

and

secondary

alarm stations,

protected

area

lighting,

protected

and vital

area

barrier

integrity,

and

the

security

organization

interface

with

operations

and maintenance.

(6)

Fire Protection

- Fire protection activities,

staffing

and

equipment

were observed

to verify that fire brigade staffing was

appropriate

and

that fire alarms,

extinguishing

equipment,

actuating

controls,

fire

fighting

equipment,

emergency

equipment,

and fire barriers

were operable.

/

The licensee's

adherence

to radiological controls, security controls,

fire protection requirements,

and

TS requirements

in these

areas

were

satisfactory.

c.

Review of Nonconformance

Reports

Adverse

Condition

Reports

(ACRs)

were

reviewed

to verify the

following:

TS were complied with, corrective actions

as identified

in the

reports

were

accomplished

or being

pursued for completion,

generic

items were identified and reported,

and

items were reported

as required

by the TS.

No violations or deviations

were identified.

3.

Surveillance

Observation

(61726)

Surveillance

tests

were observed

to verify that approved

procedures

were

being

used;

qualified personnel

were

conducting

the tests;

tests

were

adequate

to verify equipment

operability;

calibrated

equipment

was

utilized; and

TS requirements

were followed.

The following tests

were observed

and/or data reviewed:

OST-1506

Reactor Coolant System Isolation Valve Leak Test

MST-I0135 Main Steam

Feedwater

Flow Loop

1 Operational

Test

NST-I0145 Steam Generator

A Narrow Range

Level Operational

Test

NST-I0146 Steam Generator

B Harrow Range Level'Loop Operational

Test

EPT-159

EPT-183

ASNE Section XI, Article IWB-5000 102 Percent Hydrostatic

Test

1CS-744

SI Alternate Niniflow Relief Valve Relief Pressure

Test

EPT-184

1CS-755

SI Alternate Miniflow Relief Valve Relief Pressure

Test

In general,

the

performance

of these

procedures

was

found to

be

satisfactory

with proper

use of test

equipment,

necessary

communications

established,

proper

pre-test

briefings

performed,

and

knowledgeable

personnel

performed the tasks.

a ~

The inspector

observed

the

system restoration

and verification for

the

charging

alternate

miniflow relief valve test

performed

in

accordance

with section

7.2 of procedures

EPT-183

and

EPT-184.

This

section

verified that

several

system

drain

valves

and

test

connections

(ICS-745,

1CS-756,

1CS-753,

and

1CS-754)

were returned to

the

normal

system lineup.

The initial positioning of these

valves

was

performed

by plant

operating

personnel.

The

independent

verification of valve position

was

performed

by the

system test

engineer.

The inspector

also

observed

that

the

valves

had

been

positioned to the proper positions.

Since

system

engineers

were not routinely utilized for independent

verification functions, the inspector questioned

the test engineer to

ascertain

his qualifications.

He stated

that it was

a

common

practice for system

engineers

to perform this task

and that

he

had

received

appropriate

training.

Licensee

management

stated

that

although

system

engineers

receive

some training,

they

were

not

qualified to perform independent verification of components

returned

to service

but were allowed to check valve positions inside the test

boundaries

during

the

test.

In contrast,

licensee

operating

personnel

receive

specialized

training in various

techniques

of

checking

valve

positions

and

the

special

requirements

regarding

independent

verification.

The licensee

considered

the

performance

of

independent

verification

by

the

system

engineer

to

be

inappropriate.

The

licensee's

administrative

controls

regarding

performance

of

independent

verifications

are

specified

in

procedure

PLP-702,

Independent Verification.

Section 5.3.3 of this procedure lists the

guidelines

to be applied in determining which individuals may perform

independent

verifications.

These

guidelines

are

very general

in

nature

and

simply require

that

only qualified

personnel,

as

designated

by their

foreman,

be

allowed to perform

independent

verification.

The utilization of a test engineer for the performance

of the independent verifications in section 7.2 of procedures

EPT-183

and

EPT-184 is contrary to the requirements

of procedure

PLP-702

and

is considered

to be

a violation of TS 6.8. l.a.

Violation (400/92-04-02):

Failure to use

a qualified person for the

performance of independent verifications.

4.

Maintenance

Observation

(62703)

The

inspector

observed/reviewed

maintenance

activities to verify that

correct

equipment

clearances

were

in effect;

work requests

and fire

prevention

work permits,

as

required,

were

issued

and

being followed;

quality control

personnel

were available for inspection activities

as

required;

and,

TS requirements

were being followed.

Maintenance

was observed

and work packages

were reviewed for the following

maintenance

(WR/JO) activities:

Disable

the

"B" digital

rod position indication cabinet

detector

encoder

card for control

rod

H-14 in accordance

with temporary

modification PCR-6264,

DRPI

Rod H-14 Half Accuracy.

Troubleshoot

failure of electrical

distribution

breaker

1A-3 to

properly close.

Addition of oil to the "A" and "B" reactor coolant

pump motors.

Replace

regulator

on air operated auxiliary feedwater

valve

1AF-102

in

accordance

with procedure

MPT-I0002,

Ralph

A. Hiller Model

12SA-A029 Valve Actuator,

and post-maintenance

testing in accordance

with procedure

OST-1077, Auxiliary Feedwater

Valves Operability Test

quarterly Interval.

Replace

"C" phase

main transformer oil coolant

pump.

Replace

rotating

element

for the

"A" main

feedwater

pump

in

accordance

with procedure

CN-N0132,

Main

Feed

Pump

Disassembly

Inspection

and Reassembly.

Rebuild hydraulic operator for main steam

power operated relief valve

1NS-58 in accordance

with procedures

CM-M0186, Paul

Monroe Main Steam

Power Operated

Relief Valve Operator Fill and

Bleed Procedure,.

and

CM-M0188,

Main

Steam

Power

Operated

Relief

Valve

Operator

Disassembly,

Maintenance

and Reassembly.

In

general,

the

ma intenance

obser ved

was

performed

sati s factory.

Appropriate

procedures

were utilized

and

proper return to service

of

affected

components

was independently verified by the craft.

a.

The inspector

attended

the pre-job briefing for the main transformer

work.

This work was critical because it was performed with the plant

on-line

and with the transformer

remaining energized.

The work was

performed

by the licensee's

transmission

department.

The licensee's

pre-planning for this work was

thorough

and included the following

attributes:

The

work activity

and

outline of steps

was

discussed

and

approved

by the

PNSC.

Several

critical

steps

in the

process

were specified

to

be

independently verified.

Plant auxiliary loads

were placed

on the start-up

transformers

in the event of a possible turbine trip.

The fault pressure

relay associated

with the transformer coolant

pressure

was

disabled

during

maintenance

thereby

avoiding

spurious

switchyard breaker

and generator

output breaker trips.

A fire truck and fire watch

were positioned

nearby to combat

potential electrical fires.

An operator

was

assigned

to

be in constant

contact with the

control

room via radio if a problem should develop.

Practice

dry-runs were performed

on the spare transformer prior

to performing work on the

"C" main transformer.

The

licensee's

detailed

planning

and

use of mockups

were

very

effective in accomplishing

the reactor coolant

pump oil addition

and

transformer repairs without mishap

and are considered

to be strengths

in the maintenance

functional area.

b.

Circuit breaker

lA-3 (breaker

108)

experienced

reoccurring closing

problems

during this inspection period.

The breaker

supplies

power

from the unit auxiliary transformer to station unit auxiliary bus

1A.

Non-safety related

plant

loads

are

supplied

from this

bus.

On

a

loss of the main turbine/generator,

breaker

108 is required to open

and

auxiliary

bus

1A

will

automatically

switch

to

the startup

transformer

as

a

power

source

via breaker

107.

The

licensee's

troubleshooting

of this problem identified

a structural

problem in the breaker

cubicle which allows the breaker

secondary

disconnects

to disengage

and

prevent

breaker

closure.

A plant

modification

(PCR-6282,

Cubicle

lA-3 Breaker

Closing

Problem)

has

been initiated to correct

the

problem.

The inspectors

considered

this action to be appropriate.

c ~

In conjunction

with

the

observation

of the

CCW modification,

PCR-5748,

the licensee's

administrative controls regarding

the use of

freeze

plugs

was

also

performed.

The inspectors

reviewed

the

licensee's

procedures

for installing freeze

plugs in piping, training

records of personnel

trained

on the

use of freeze

plugs,

the freeze

plug training lesson

plan,

and visited the hands-on training facility

for freeze

plug installation.

Guidance

provided in

NRC Inspection

Manual, Part

9900 was utilized during this inspection.

Freeze

plugs

were

usually

installed

by

the

plant

services

organization.

For the

CCW modification, several

good pre-evolution

planning

practices

were

observed,

as

discussed

in

NRC Inspection

Report 50-400/92-02.

However,

the procedure utilized for installing

the

freeze

plugs,

MMP-012, Hydrostatic

and

Pneumatic

Testing of

Piping

Systems,

lacked

several

important features

including freeze

plug temperature

monitoring specifics,

nitrogen

source

requirements,

and contingency planning.

The good pre-planning for this work offset

the shortcomings of the procedure.

The licensee's

maintenance

organization also

had

a separate

procedure

for installing

freeze

plugs.

Recently,

these

procedures

were

combined

into

a single

procedure for all work groups

to use

when

installing freeze

plugs.

The

new procedure

incorporated

industry

lessons

learned

from

events

at

other

nuclear

stations.

The

inspectors

found that the recently revised

procedure

CM-M0169, Freeze

Seal

Procedure,

specified

appropriate

steps,

precautions,

and

limitations for installing

freeze

plugs.

The

procedure

also

incorporated

most of the guidance

provided in

NRC Inspection

Manual

Part

9900.

The inspectors

noticed that the

new procedure

did not

specifically address

communications

requirements

between

the control

room

and

the

personnel

performing

the

work.

The

extent

of

communication

was left up to the desires

of the operating shift to

specify.

The inspector

considered

a more formal requirement

to be

appropriate.

The

new procedure

also lacked specific provisions for

moni toring nitrogen flow.

The licensee

considered

observation of the

gaseous

plume

and

a level

indicated

in the jacket

annulus

to

be

sufficient.

The inspector

informed the licensee that this might not

be sufficient to positively verify nitrogen flow which is necessary

to maintain

freeze

plug integrity.

The

new procedure

specified

contingency

actions if the

seal

failed.

Thi's action

would

be

specified

for

each

individual

seal

and

would

reference

the

appropriate

emergency

procedure for the loss of the affected

system.

The

inspector

discussed

these

observations

with the licensee

who

stated that appropriate

procedure

revisions

would be considered.

The licensee

has trained

one

crew of plant services

and three plant

maintenance

crews

on the

use

and installation of freeze

seals

using

the

new

procedure.

The

inspectors

found this training to

be

thorough.

No violations or deviations

were identified.

10

Safety

Systems

Walkdown (71710)

The inspector

conducted

a walkdown of the

emergency

service water system

to verify that the lineup was in accordance

with license requirements for

system operability

and that the

system

drawing

and

procedure

correctly

reflected "as-built" plant conditions.

The general

material

condition of the system

was found to be satisfactory

except for some general

corrosion found

on the yokes of several

instrument

root

and drain valves.

Additionally, the inspector

noted

a discrepancy

between

the

system

drawing

and the as-built plant conditions in that the

drawing reflected only one of two valves in series

on a drain line.

These

findings

were

referred

to the

system

engineer

for corrections.

The

deficiencies

did not affect system operability.

No violations or deviations

were identified.

Review of Plant Nuclear Safety Committee Activities (40500)

The

inspectors

attended

selected

PNSC

meetings

to

observe

committee

activities

and

verify

TS

requirements

with respect

to

committee

composition,

duties,

and responsibilities.

Minutes from these

meetings

were

also

reviewed

to verify accurate

documentation.

The inspector

considered

the

conduct

and

documentation

of these

meetings

to

be

satisfactory.

During the

PNSC

meeting

on

February

18,

maintenance

activities to repair

a coolant

pump for the

"C" phase

main transformer

were discussed.

Specific guidelines

were presented

which described

the

replacement

effort

and

potential

independent

verification steps

were

identified.

The

committee

decided

that this work could

be

performed

safely

with the

plant

online.

No violations

or deviations

were

identified.

Review of Spent

Fuel Handling Activities (71707)

As previously mentioned

in

NRC Inspection

Report 50-400/91-22

and 50-400/

91-01, the licensee

was in the process

of cleaning

up the spent fuel pools

and transfer

canals

utilizing an

underwater filter and

vacuum unit.

During this reporting period,

licensee

management

met with the inspectors

to discuss

future plans

on fuel shipments

and cleanup of the crud located

on the bottom of the spent fuel pools.

Due to significant area

radiation levels

associated

with the underwater

filters

and potentially high personnel

exposures

when handling/changing

out the filters, licensee

management

has reevaluated

the potential nuclear

safety

and

radiological

concerns

between

the

crud

cleanup

and

the

alternative

consequences

of leaving the crud

on the bottom of the pools,

and

has

decided to leave

the crud in the pools.

Based

on the tendency of

the

crud

to

remain

on

the

bottom of the

pools

unless

agitated

significantly,

and little intersystem

communication

between

the spent fuel

and

RC systems

during refueling operations,

the licensee

believes

the crud

hazard

can

be administratively controlled until plant decommissioning.

This action would allow time for the natural

decay of radioactive

isotopes

before

any

cleanup effort which would significantly reduce

personnel

exposure.

Licensee

personnel

have performed

an accident analysis

assuming

a

maximum crud loading in the spent fuel pools.

The licensee

plans to

maintain the crud concentration

within this analysis

and

does not plan to

process

spent

fuel

system

water

with the

radwaste

system

thereby

minimizing the effect

on other plant systems.

Furthermore,

most work

activities which generated

the radiological

problems in the past for pool

draindown,

rack installation,

and weld repairs,

have

been completed.

Only

minor reracking activities are planned in the future.

Although licensee

management

philosophy

addressed

previous

NRC concerns,

specific procedural

precautions

have not

been

implemented.

Nore formal

administrative controls for minimizing the spread of the crud hazard

were

recommended.

Short

Duration

Outage

to Repair

RTD

Bypass

Manifold Isolation

Valve

(71707)

On February

29,

1992,

a

power reduction

was

performed to secure

the "A"

main feedwater

pump.

Operating

personnel

noticed

excessive

vibrations

on the

pump balancing flow line.

While the plant was at

a reduced

power

level,

licensee

management

decided

to initiate repairs

to the

"C" main

transformer

and to add oil to "A" and "B" reactor coolant

pump motors.

During the oil addition to the reactor

coolant

pumps,

plant personnel

noticed

evidence

of boric

acid

leakage

from valve

1RC-22,

inside

containment.

Licensee

management

conservatively

decided

to shutdown

the

plant

and effect repairs

even

though

the

leakage

was well within TS

limits.

An additional

valve

(1RC-953)

adjacent

to

1RC-22

was

also

leaking.

The plant was

taken to hot shutdown

(Node 4) to effect repairs.

Both valves

were repaired

by installing

a valve cap over the valve stem.

Following this maintenance

work,

a plant heatup

and startup

were performed

and

the plant

resumed

power operation

on

March

12.

The inspectors

witnessed

the shutdown,

cooldown,

heatup,

and startup activities

and also

were present

when the reactor

was taken critical.

Implementation of the

following plant procedures

was observed:

GP-002

Normal Plant Heatup from Cold Solid to Hot Subcritical

Node

5 to Node 3.

GP-004

Reactor Startup

(Node

3 to Mode 2).

GP-006

Normal Plant Shutdown from Power Operation to Hot Standby

1

to Mode 3;

GP-007

Normal Plant Cooldown

(Node

3 to Mode 5).

12

This

shutdown indicated

licensee

management's

support for the control of

boric acid corrosion.

Prompt repair of the leaking valves,

instead of

waiting

to

the

next refueling

outage,

was

prudent

and

prevented

unnecessary

repairs

which could have arisen

from the effects of boric acid

corrosion.

Outage

planning

was

detailed

and

properly

implemented.

Operation of the plant to achieve

the necessary

status

was satisfactory.

However,

a

rod position indication

problem which occurred

during both

shutdown

and startup operations

caused

a slight delay in reactor startup

activities

on March 12.

The problem,

which affected position indication

for control

rod B-10 at the 24-step elevation,

had originally caused

the

"RPI Urgent Alarm" to annunciate

on March

7 during plant shutdown.

At

that time, operators

did not troubleshoot

the occurrence

or initiate

a

work request

but continued

on with the plant shutdown.

When the event

reoccurred

during the plant startup,

a work request

was

generated

as

required

by Annunciator

Panel

Procedure,

APP-ALB-013, Main Control Board.

Such actions

on March

7 would have eliminated the delay

when the problem

recurred

during startup.

No violations or deviations

were identified.

Design

Changes

and Modifications (37828)

Installation of new or modified systems

were reviewed to verify that the

changes

were reviewed

and

approved

in accordance

with 10 CFR 50.59, that

the

changes

were

performed

in

accordance

with technically

adequate

approved

procedures,

that

subsequent

testing

and test

results

met

acceptance

criteria or deviations

were resolved

in an acceptable

manner,

and that appropriate

drawings

and facility procedures

were revised

as

necessary.

This review included

selected

observations

of modifications

and/or testing

in progress.

The following modifications/design

changes

were reviewed:

PCR-6265

Leak Repair of 1RC-22

PCR-6273

Leak Repair of 1RC-953

PCR-5748

CCW Thermal Relief Valve Deletion

PCR-5741

CCW From SFP Coolers

Low Flow Alarm, Excess

Letdown Design

Pressure

Uprate.

Modifications

PCR-6265

and

PCR-6273 installed valve caps

over the valve

stems

and

removed the associated

valve operating

handles.

The valves were

verified to be

open

and

then the

caps

were welded

on to prevent leakage.

The performance of these modifications

was found to be satisfactory.

a.

Modification

PCR-5741

raised

the relief setpoint for the

excess

letdown

heat

exchanger

relief valve to allow higher

CCW system

operating

pressure.

This modification, in conjunction with PCR-5748,

was

performed

to allow normal

CCW operation

at higher

pressures

Ci

13

without lifting system relief valves

as

described

in

LER 90-18.

Subsequent

modeling of the

CCW system

by licensee

design

engineers

revealed

that the completed modifications would still not suffice to

allow

normal

system

operations

and

that

additional

plant

modifications

would

be

necessary.

The

licensee

is presently

evaluating

design

change alternatives.

Although these modifications

removed

several

system relief valves

which will minimize potential

inventory loss

from the

CCW system during pressure

spike transients,

the

inspectors

considered

the

scope

of the modifications

to

be

insufficient to achieve

the desired

goal

which was to return the

system to

a normal configuration.

During

a review of control

room drawings

on February

28,

1992,

the

inspector

noticed that drawings

2165-S-1320

and

2165-S-1322

did not

depict the modifications

which

had

been

performed

on the component

cooling water

system

to replace

heat

exchanger relief valves with

small

flow orifices

(PCR-5748).

Due to the large extent of this

modification,

the

various

CCW heat

exchangers

were

modified in

stages.

The two

RHR and

BRS heat

exchanger

CCW modifications were

field completed

and

the

system

turned

over

as functional to plant

operations

on November 20,

December

4,

and January

16, respectively.

Usually plant drawings

are updated with modification status

by use of

red-lines until final drawing revisions

are

produced.

A review of

the clearance

center

drawings revealed similar discrepancies.

The discrepancies

were

discussed

with plant operations

management

personnel.

Their investigation

revealed

that the drawings

had

been

annotated

with the correct modification information but subsequent

drawing revisions

had

been

produced

which replaced

the red-lined

drawings.

Although the replacement

drawings included previous plant

modifications

to

the

system,

the relief

valve

replacement

modification had not yet been

included.

This detail

was overlooked

by the operations

production assistants

when replacing the drawings

and

the red-line information

was

not included

on the

new drawing

revisions.

Licensee

personnel

previously recognized

the potential

for this

problem to occur

and

prepared

a

procedure

revision to

require

a comparison

between old red-lined drawings

and

new revisions

to verify that all red-line information is included

on new drawings.

As of February

28, the procedure revision

had not been

implemented.

A previous

problem with failure to update plant drawings for modified

systems

was identified in

NRC Inspection

Report

50-400/91-09

in May

1991,

which resulted

in

a violation (400/91-09-01).

The licensee's

corrective

action for this violation included detailed

procedural

guidance

for the

operations

production

assistants

and

an audit

process

to

review

the

red-lined

drawings

quarterly

and at

the

completion of major outages.

The inspector

requested

the last audit

performed

but was

informed

by the licensee

that the audits

had not

been

performed

as required.

The licensee's

corrective actions

were

considered

incomplete

and

inadequate.

Failure

to

perform

comprehensive

and

complete

corrective

action is contrary to the

'

14

requirements

of

10 CFR 50,

Appendix

B, Criterion

XVI, and is

considered

to

be

an additional

example of the violation discussed

in paragraph

2.a.( 1) of this report.

When informed of this finding, licensee

personnel

completed

an audit

of the drawings

and found numerous additional errors.

10.

Review of Licensee

Event Reports

(92700)

The following LERs were reviewed for potential

generic

impact, to detect

trends,

and to determine

whether corrective actions

appeared

appropriate.

Events that were reported

immediately

were reviewed

as they occurred to

determine if the

TS were satisfied.

LERs were reviewed in accordance

with

the current

NRC Enforcement Policy.

a

~

b.

(Open)

LER 92-02:

This

LER reported

the undetected

failure of the

plant computer which resulted in a violation of the TS.

The licensee

has corrected

the specific problem with the operation of the computer

program

and is planning

computer

upgrades

to increase reliability.

Also, operating

procedures

will be

enhanced

to provide additional

details

on computer

TS related functions.

The

LER will remain

open

pending

completion

of

the

computer

upgrade

and

procedure

enhancements.

(Closed)

LER 92-03:

This

LER reported that the hot leg recirculation

switchover time specified

in plant emergency

procedures

and the

FSAR

was

incorrect.

This matter

was identified

by the

nuclear

steam

system

supplier during the review process

for a proposed

technical

specification

change.

The

licensee

has

revised

the

emergency

procedures

and

has

approved

a revision to the

FSAR to reflect the

correct time.

11.

Exit Interview (30703)

The inspectors

met with licensee

representatives

(denoted

in paragraph

1)

at the

conclusion

of the inspection

on

Harch

20,

1992.

During this

meeting,

the

inspectors

summarized

the

scope

and

findings of the

inspection

as they are detailed in this report, with particular

emphasis

on

the

violations.

The

licensee

representatives

acknowledged

the

inspector's

comments

and

did not identify as

proprietary

any of the

materials

provided

to

or

reviewed

by

the

inspectors

during this

inspection.

Item Number

400/92-04-01

Descri tion and Reference

Violation -

Failure

to

proper ly identi fy

and

correct

deficiencies

a

required

by

10 CFR 50,

Appendix

B,

Criterion XVI, paragraph

2.a. (1) and 9.b.

15

400/92-04-02

Acronyms and

Violati on -

Failure

to

use

a

qual ified

person

for

performance of independent verifications,

paragraph

3.a.

Initial i sms

ACR

AFW

ALARA

ASME

BRS

CCW

CFR

DRPI

EPT

FSAR

HVAC

LER

MPT

MST

NCV

NRC

OST

PCR

PLP

PNSC

RAB

RCP

RCS/RC

RHR

RTD

RWP

SFP

SI

TS

WR/JO

Adverse Condition Report

Auxiliary Feedwater

As Low As Reasonably

Achievable

American Society of Mechanical

Boron Recovery

System

Component

Cooling Water

Code of Federal

Regulations

Digital Rod Position Indication

Engineering

Performance

Test

Final Safety Analysis Report

Heating, Ventilation and Air Co

Licensee

Event Report

Maintenance

Performance

Test

Maintenance

Surveillance Test

Non-Cited Violation

Nuclear Regulatory

Commission

Operations

Surveillance Test

Plant

Change

Request

Plant Program Procedure

Plant Nuclear Safety Committee

Reactor Auxiliary Building

Reactor

Coolant

Pump

Reactor Coolant System

Residual

Heat

Removal

Resistance

Temperature

Detector

Radiation

Work Permit

Spent

Fuel

Pool

Safety Injection

Technical Specification

Work Reque8st/Job

Order

Engineers

nditioning