ML17317A719

From kanterella
Jump to navigation Jump to search
Notice of Violation from Inspec on 780829-01
ML17317A719
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 10/04/1978
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17317A718 List:
References
50-316-78-22, NUDOCS 7811090185
Download: ML17317A719 (4)


Text

A endix A NOTICE OF VIOLATION American Electric Power Service Corporation Indiana and Michigan Power Company Docket No. 50-316 Based on the inspection conducted on August 29-Septem ber 1

1978 it ha certain of your activities were in noncompliance with appears t at cer a n o NRC requirements, as noted below.

Items 1 t roug are n r and item 4 is a deficiency.

Technical Specification 3.7.1.2 requires when in Modes 1, 2 and 3 that an inoperable auxiliary feedwater pump be restored to operable status within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or the plant be in Mode 4 within the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />'.

2 ~

Contrary to e a v,

t th above results of the turbine driven auxiliary f

d t r pump surveillance test conducted on June ee wa er u

ndicated secor ance w

d ith Technical Specification 4.7.1.2.a.l indic the pump to be inoperable with the plant in o

e an action required by Technical Specification 3.7.1.2 was not taken.

T h ical S ecification 4. 5.2.f.l requires that the centrif-ec n ca pe month b uga c arg n 1

h r ing pump be demonstrated operable every y

> 2405 si ver y ng if i the indicated discharge pressure to be p

g 4.0.5 during testing required by Technical Specification (ASME Section XI testing).

C t

the above testing conducted on April 1 1 1978 as f dis-required by Technical Specification 4.0.5 did not veri y s-re to be

> 2405 psig due to a leaking pressure charge pressure to e

o conducted after au e (QPI-253) coupling and retesting was not conduc e

a corrective maintenance was completed on the gauge p

e cou lin on April 12, 1978.

3.

Technical Specification 4.0.5 requires inservice testing of ASME Code Class 1,

2 and 3 pumps be performed in accordance with Section XI of the ASME Boiler and Pressure Vessel Code

. 1974 Edition and Addenda through Summer 1975.

Appendix A Contrary to the above, a.

Records of inservice tests for the period J y

anuar 20, 1978 ch 3 1978 did'not include the identification w ble ran es of of instruments

used, comparisons with allowa g

test values and analysis of deviations as required by Section XI, Subarticle IWP-6240.

c ~

R d

of inservice tests performed during the month of ecor s

March 1978 on ECCS Train B were not accessible as q

as re uired by Sectio~ XI, Subarticle IMP-6260.

The August 22, 1978 results of a component cooling water pump 2M test an t e ugus d

h A

st 8

1978 results of an essential service water pump 2E test were in the "Required Action bl IMP-3100-2 of ASME Code Section XI and the pumps were not declared inoperable as required by Section le IMP-3230.

Several other examples were noted e" of Table w ere es h

e test results were in the "Alert Range o

a e

IMP-3100-2 and testing frequencies were not o

not doubled as required by Subarticle IWP-3230.

4 Technical Specification 6.5.2.10.a requirees minutes of each NSDRC meeting be prepared, approved and fo and forwarded to the Senior Execut ve ce r

Vi P esident Engineering and Construction, AEPSC, within 14 days following each meeting.

h b

e the minutes of NSDRC Meeting No.

18 con-Contrary to t e a ove, e

d and forwarded ducted on April 6, 1978 were not prepared, approved and until July 18, 1978.