ML16342D971

From kanterella
Jump to navigation Jump to search
Insp Repts 50-275/97-23 & 50-323/97-23 on 971123-980103.No Violations Noted.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support
ML16342D971
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 01/26/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML16342D972 List:
References
50-275-97-23, 50-323-97-23, NUDOCS 9802050357
Download: ML16342D971 (38)


See also: IR 05000275/1997023

Text

ENCLOSURE

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket Nos.:

50-275

50-323

License Nos.:

DPR-80

DPR-82

Report No.:

Licensee:

Facility:

Location:

50-275/97023

50-323/97023

Pacific Gas and Electric Company

Diablo Canyon Nuclear Power Plant, Units

1 and 2

7 1/2 miles NW of Avila Beach

Avila Beach, California

.

Dates:

Inspectors:

Approved By:

November 23, 'l997 through January 3, 1998

David L, Proulx, Senior Resident Inspector

Donald B; Allen, Resident Inspector

Brad J. Olson, Project Inspector,

Region IV

Howard J. Wong, Chief, Reactor Projects Branch E

ATTACHMENTS:

Attachment 1:

Supplemental

Information

'7802050357

980126

PDR

ADQCK 05000275

8

PDR

0

-2-

EXECUTIVE SUMMARY

Diablo Canyon Nuclear Power Plant,:Unit's

1 and 2

NRC Inspection Report 50-275/97023; 50-323/97023

This inspection included aspects of licensee operations,

maintenance,

engineering,

and

plant support.

The report covers

a 6-week period of resident inspection.

~Qerarione

Work planning for control room painting warranted improvement because

the

configuration of the control room ventilation, the location of the compressor,

and

the effects of the painting on the control room charcoal filters were not formally

preplanned

or analyzed.

Operators took prudent and conservative

action to

minimize distractions and mitigate the effects of fumes in the control room during

the painting (Section 02.1).

inadve

Maintenance

A noncited violation was identified for failure to maintain the design basis of an

auxiliary feed pump.

A ventilation flow path for the auxiliary feed pump rooms was

rtently blocked (Section 08.3).

Auxiliary Salt Water (ASW) vault check valve maintenance

did not include a post

maintenance

test to demonstrate that the valve was installed properly.

However,

the task was performed properly in accordance

with the work order. (Section

M1.2).

Surveillance tests observed were performed well (Rection M1.3).

Plant material condition was generally good and continued to improve during this

inspection period.

Minor leaks and concerns were noted such as leaking centrifugal

charging pumps, leaking electro-hydraulic control fluid on Unit 1, and degraded

Unit 2 turbine end seals (Section M2.1).

~

A noncited violation was identified with three examples of failure to implement

surveillance requirements

(Section M8).

~ncnineering

Engineering personnel provided

a timely and technically sound response

to concerns

with the design basis of the plant's response to a spurious safety injection signal

(Section E1.1).

0

-3-

The operability evaluation associated

with containment fan cooler unit motor

cracked welds was technically sound and had good engineering

basis

(Section E2.1).

Routine personnel radiation practices were performed well (Section R1.1).

Routine security practices were performed well (Section S1.1).

0

-4-

Re ort Details

Summer

of Plant Status

Unit 1 began this inspection period at 100 percent power.

Unit

1 continued to operate at

essentially 100 percent power until the end of this inspection period.

Unit 2 began this inspection period at 100 percent power.

Unit 2 continued to operate at

essentially 100 percent power until the end of this inspection period.

I. ~Qerations

Q1

Conduct of Operations

0'l.l

General Comments

71707

The inspectors visited the control room and toured the plant on a frequent basis

when on site, including periodic backshift inspections.

In general, the performance

of plant operators was professional

and reflected a focus on safety.

Operators

continued to perform well in utilizing three-way communications,

and operator

responses

to alarms were observed to be prompt and appropriate to the

circumstances.

Limiting conditions for operation were properly entered,

as required.

02

Operational Status of Facilities and Equipment

02.1

Paintin

Control Room Panels

a.

Ins ection Sco

e 71707

The inspectors evaluated the licensee's

planning and execution of painting of the

control room electrical panels to ensure that this evolution did not adversely impact

safe operation of the facility.

b.

Observations

and Findin s

On December 31, 1997, the inspectors

noted that the licensee was preparing to

paint the lower skirts of the control room main control board panels.

This evolution

was to be done by hand using sprayers.

The inspectors were concerned

that the

paint would introduce fumes that would affect the operators

and cause the control

room ventilation system charcoal filters to become inoperable.

In addition, the

inspectors were concerned that paint spray could cause control room instruments to

be inoperable and the noise of the sprayers could distract the operators from their

licensed duties.

-5-

The inspectors discussed

the licensee's

plans with the operations

manager.

The

operations

manager provided the inspectors with copies of the risk assessment

and

work order C0155269 associated

with the job.

The risk assessment

stated that

preparations for and painting of the control boards was considered

a high risk job.

For contingencies,

the risk assessment

required

a briefing of the workers, an

operations walkdown with the work crew, and the supervisor to check-in with the

shift foreman.

In addition, the painters employed

a water-based

rather than enamel

paint to minimize the effect of fumes on the control room envelope.

This action

was taken in response to a 1995 action request in which paint fumes became

intolerable to the point of several operators having to exit the control room for fresh

air. The inspectors considered the licensee's preparations

to be acceptable with the

following concerns.

The inspectors asked the operations manager how the licensee had analyzed the

effect of the painting on the operability of the control room emergency filtration

charcoal filters. The licensee stated that they would perform an after-the-fact

evaluation should the system inadvertently actuate.

The inspectors considered this

to be nonconservative

because

volatile organic compounds

found in most paints

were known to be detrimental to charcoal filtration.

The licensee noted that certain aspects of the task were not formally documented

in

the work plan.

The work plan did not address the location of the compressor for

the paint sprayers.

At the start of the job, the paint crew planned to locate the

compressor

such that control room doors would be propped open.

The shift

supervisor rejected this plan, and instead the compressor was relocated to the shift

supervisor's office with the lines to the sprayers running under the door.

The

inspectors noted that this configuration precluded propping open any doors and kept

the noise to a minimum.

In addition, the work order or risk assessment

did not

formally discuss methods to remove fumes.

Prior to the task, operators placed the

control room envelope

in mode 2 operation which provides 100 percent makeup of

outside air. This action minimized the effect of fumes on control room personnel.

The inspectors noted that the painting activities were executed well overall.

The

inspectors concluded that although operators took prudent and conservative

action

to minimize distractions in the control room, and mitigate the effects of fumes, the

work planning warranted improvement because

the configuration of the control

ventilation and the location of the compressors

occurred just prior to work initiation

and should have been considered

in the work planning process.

Conclusions

Work planning for control room painting warranted improvement because

the

configuration of the control room ventilation, the location of the compressor,

and

the effects of the painting on the control room charcoal filters were not formally

preplanned

or evaluated.

Operators took prudent and conservative

action to

minimize distractions and mitigate the effects of fumes in the control room during

the painting.

-6-

08

Miscellaneous Operations Issues (92700;.92901)

08.1

,

08.2

Closed

Violation 50-275 96019-02:

failure to report off clearance prior to

removing ground buggies.

This violation was cited for not following procedures

when removing ground buggies from 4 kV auxiliary feeder breakers.

As a result of

this occurrence,

and more significantly, an October 1995 event in which an

auxiliary transformer failed due to improper installation of ground buggies, the

licensee implemented new controls for the use ground buggies.

The licensee

revised procedures

for clearances

and tag-outs, electrical maintenance,

and

energization of electrical busses.

As documented

in NRC Inspection Reports

50-275/97-01

and 50-275/97-06, inspectors observed

actions to re-energize

electrical buses during a Unit

1 refueling outage.

The licensee's

actions were

performed using the revised process for the control of ground buggies,

The

inspectors observed that the activities were performed in a deliberate manner, with

self and peer-checking

evident.

The inspectors

also documented that the operators

were well aware of how inadequate

ground buggy control led to the failure of an

auxiliary transformer.

During this inspection period, the inspectors reviewed the

procedure changes

made for the control of ground buggies.

The inspectors

had no

additional comments regarding the licensee's corrective actions.

Closed

Violation 50-323 96-009-01'and

Licensee Event Re ort

LER 50-275 95-

006-00:

loads moved over the spent fuel pool'with the ventilation system not

capable of being powered automatically from an operable emergency power source.

The violation was issued after multiple instances

where the licensee did not

maintain the fuel handling building ventilation system operable when required by

Technical Specifications.

Included in these instances was an event described

in

LER 50-275/95-006-00.

The licensee determined &at the root causes of the events

were somewhat different, but all were attributed to personnel

errors.

As corrective

actions for the violation and the LER, the licensee counseled

personnel,

provided

lessons

learned,

and changed procedures to ensure that emergency power was

available to the ventilation systems.

The inspectors noted that the licensee had not

experienced

a recurrence of this problem during recent refueling outages.

The

inspectors reviewed the licensee's corrective actions and found them acceptable.

(

08.3

Closed

LER 50-275 96-009-00:

auxiliary feedwater pump inoperable due to

inadvertent blockage of a ventilation flow path.

This LER was submitted after the

licensee discovered

a steel plate blocking the ventilation path from the turbine drive

auxiliary feedwater pump room.

The licensee removed the steel plate and

determined that the condition could have caused the environment in the room to

exceed conditions assumed

in the steam line break analysis.

The licensee reviewed

other ventilation flow paths to identify hatches

or grates which could be readily

blocked and affect air flow required to meet plant or system operation.

The licensee

installed signs to warn personnel not to'block the identified hatches

or grates.

The

inspectors reviewed the licensee's corrective actions and verified the installation of

signs.

The inspectors found the licensee's corrective actions to be acceptable.

-7-

Failure to maintain the design basis of the auxiliary feed pump is a violation of

10 CFR Part 50 Appendix B, Criterion III. However, this licensee-identified

and

corrected violation is being treated as a noncited violation, consistent with

Section VII.B.1 of the NRC Enforcement Policy (50-275/97023-01).

II. Maintenance

M1

Conduct of Maintenance

M1.1

Preventative Maintenance

on Solenoid Tri

Box Unit 2

a.

Ins ection Sco

e 62707

The inspectors observed

portions of work orders AT MM AR0443341, C0155045,

and C0152077, "Remove Turbine Trip Solenoid Box" and

"Inspect and Lubricate

Trip and Throttle Valve for Auxiliary Feed Water Pump 2-1."

b.

Observations

and Findin s

Maintenance

personnel were knowledgeable

of the equipment, procedures,

and

tasks to be performed.

The work documents

and applicable procedures

were at the

work site, and were used and signed as the work progressed.

The system engineer

was present and assisted

in the removal of the turbine trip solenoid box, which had

been abandoned

in place.

Clearance tags were hung to protect the equipment and

personnel.

C.

Conclusions

'0

The maintenance

activities were performed in accordance

with the procedural

requirements.

The personnel performing the activity were knowledgeable

of the

equipment, procedures,

tools and methods used.

The results of the maintenance

appeared to be effective in ensuring the components

willfunction as designed.

M1.2

ASW Vault Check Valve Preventive Maintenance

Unit 1

a.

Ins ection Sco

e 62707

The inspectors observed performance of work order RO177189, "ASW Vault Check

Valve SW-2-9881nspection

and Preventative Maintenance."

b.

Observations

and Findin s

NRC Inspection Report 50-275;323/97014

discussed

issues associated

with

improper maintenance

of the ASW vault check valves.

The inspectors noted in that

report that the preventative maintenance

task of cleaning and inspecting these

valves revealed the valves to be frequently stuck open.

Because these valves were

0

-8-

part of the design basis to mitigate flooding in the intake structure, the valves were

considered

important to safety.

Part of the corrective actions for this previous

concern included more frequent valve inspections

and improvements to the work

procedure.

On December 31, 1997, the inspectors

noted that the work order required a flush

of the ASW vault drain piping while the valve was removed from the system for

cleaning and inspecting.

The inspectors noted that this was an improvement

because

the flushes had previously been performed following reinstallation of the

check valves.

Performing the flushes following reinstallation may have resulted in

debris being lodged in the valve internals and rendering the check valves inoperable.

During the valve inspection, the inspectors noted only sedimentation

in the valve

internals, which was documented

in the work package by the system engineer.

This minor sedimentation

did not appear to render the valve inoperable.

Following

valve inspection and cleaning, the mechanics

installed the valve and tightened the

flange nuts properly.

After completion of the work, the inspectors noted that the work package

did not

contain a post maintenance test.

The inspectors discussed

this concern with the

system engineer and the supervisor.

The licensee considered that no additional

information could be gained by a post maintenance test because

of the redundant

verification of proper valve installation.

In addition, the licensee stated that if the

check valves were installed backwards, operators would have ample time to

respond to any potential flooding that could affect the ASW pumps.

The inspectors

noted that draining water through the ASW vault drain lines as a post maintenance

test would demonstrate

that the valves were installed properly to provide additional

assurance

that the valves were operable.

I icensee management

agreed with the

inspectors'oncerns

and indicated that the procedure would be changed to include

a post maintenance

test,

c.

Conclusions

Auxiliary Salt Water (ASW) vault check valve maintenance

did not include a post

maintenance

test to demonstrate

that the valve was installed properly.

However,

the task was performed properly in accordance

with the work order.

M1.3

Surveillance Observations

a.

Ins ection Sco

e 61726

(

Selected surveillance tests required to be performed by the Technical Specifications

were reviewed on a sampling basis to verify that:

(1) the surveillance tests were

correctly included on the facility schedule;

(2) a technically adequate

procedure

existed for the performance of the surveillance tests; (3) the surveillance tests had

0

-9-

been performed at a frequency specified in the Technical Specifications;

and (4) test

results satisfied acceptance

criteria or were properly dispositioned,

The inspectors

observed

all or portions of the following surveillances:

~

STP M-9I

Diesel Generator Testing Frequency Determination, Revision 12

~

STP M-9A

Data Sheet - Routine Surveillance Test of Unit 1 Diesel

Generators,

dated 10/1/97

STP'V-3R5

Exercising Steam Supply to Auxiliary Feedwater

Pump Turbine

Stop Valve, FCV-95, Revision 10

STP M-16N1 Slave Relay Test for Operation of Interposing Relays for FCV-

95 (K632AX and K632BX), Revision

1

b.

Observations

and Findin s

Prior to the performance of Procedure

STP M-9A, operations performed a briefing in

the control room,

The briefing was thorough, covering the purpose of the test,

expected results, interface and communications with personnel at the diesel

generator,

precautions

and limitations, as well as the significant procedural steps.

The operators performed well in coordinating their timing of the diesel start

parameters to determine minimum operating parameters

of speed, frequency, and

voltage.

The steam supply to the auxiliary feedwater pump turbine Valve FCV-95 was

exercised

as directed by the surveillance Procedure

STP V-3R5. The operator

performing the test was knowledgeable

of the equipment operation and procedural

requirements.

The operators properly documented

the test results, which

demonstrated

that the valve stroke time met the test requirement.

c.

Conclusions

The inspectors found that the surveillances

observed were being scheduled

and

performed at the required frequency.

The procedures

governing the surveillance

tests were technically adequate

and personnel performing the surveillance

demonstrated

an adequate

level of knowledge.

The inspectors noted that test

results appeared

to have been appropriately dispositioned.

0

-10-

M2

Maintenance and Material Condition of Facilities and Equipment

M2.1

Plant Material Condition

a.

lns ection Sco

e 62707

During this inspection period, the inspectors conducted routine plant tours to

evaluate plant material condition.

b.

Observations

and Findin s

Centrifugal Charging Pumps;

The inspectors noted that each of the

centrifugal charging pumps on both units had noticeable oil leaks.

These oil

leaks were documented

and tracked by the licensee for correction.

None of

these leaks posed operability concerns.

Electro-hydraulic Control System:

The inspectors noted minor fluid leakage

near the front standard of the Unit 1 main turbine.

The licensee had

previously identified and documented

these leaks, and was periodically

adding electro-hydraulic control fluid to keep up with the leak.

These leaks

were scheduled to be repaired during outage

1R9.

Turbine End Seals:

The Unit 2 turbine end seal was degraded

and the

licensee was frequently monitoring its condition.

This item was scheduled to

be worked during outage 2R8.

Further degradation of this system could lead

to an unscheduled

shutdown of Unit 2.

'0

Although the inspectors observed

some material condition issues,

as described

above, the inspectors noted that licensee management

continued to properly focus

on improving the overall material condition of the facility and on reducing the

maintenance

backlog.

C.

Conclusions

Plant material condition was generally good and continued to improve during this

inspection period.

Minor leaks and concerns were noted such as leaking centrifugal

charging pumps, electro-hydraulic control fluid, and degraded

Unit 2 turbine end

seals, which were entered

and tracked in the licensee's work management

system.

M8

Miscellaneous Maintenance issues f92700, 92902)

lII

M8.'l

Closed

LER 50-275 96-002-00:

Technical Specification 3.6.1.1 not met due to

personnel

error.

This LER was based on the failure to complete

a routine monthly

check of containment isolation valves due in part to the failure to adequately

communicate

the incomplete status of parts of a surveillance test.

The licensee

0

-1 1-

attributed the cause of the missed surveillance to personnel

error in that an operator

failed to verify proper completion of a procedure.

The licensee counseled

the

individuals involved in this issue and issued an incident summary to all operating

crews.

The inspectors reviewed the licensee's corrective actions and found them

acceptable.

The inspectors considered this item to be an isolated occurrence

and

not programmatic in nature.

This licensee-identified

and corrected violation is being

treated as a noncited violation, consistent with Section VII.B.1 of the NRC

Enforcement Policy (NCV 50-275/970230-02,

Example 1),

M8.2

Closed

LER 50-275 96-004-00:

Technical Specification 3.3.3.5 not met due to

personnel

error.

This LER was based on the failure to complete

a routine

verification of the capability of each control circuit and transfer switch for the hot

shutdown panel.

The licensee attributed the cause of the missed surveillance to

personnel error in that a shift technical advisor thought the surveillance had been

completed and incorrectly marked procedure steps as not applicable.

The licensee

counseled the individuals involved in this issue and generated

recurring task work

orders to ensure verification of future surveillances.

The inspectors reviewed the

licensee's corrective actions and found them acceptable.

The inspectors considered

this item to be an isolated occurrence

and not programmatic in nature.

This

licensee-identified

and corrected violation is being treated as a noncited violation,

consistent with Section VII.B.1 of the NRC Enforcement Policy (NCV 50-

275/97023-02,

Example 2).

M8.3

Closed

LER 50-275 85-043-00:

Technical Specification 3.3.2 was not met due to

an inadequate

procedure.

This LER was submitted after the licensee determined

that containment purge valves had been opened numerous times without a current

valid slave relay test.

The licensee made their determination after reviewing a

surveillance test procedure

and finding that engineering

personnel

had failed to

include the requirement for the slave relay test.

The licensee also determined that,

although the slave relay test had not been performed, the valves were operable

and

would have closed to provide containment isolation, if required.

As corrective

action, the licensee revised surveillance procedures

to test the containment isolation

function prior to entering refueling outages

and to perform timing tests of isolation

valves on a quarterly basis.

The inspectors reviewed the licensee's corrective

actions and found them to be acceptable.

The inspectors considered this item to be

an isolated occurrence

and not programmatic

in nature.

This licensee-identified

and

corrected violation is being treated'as

a noncited violation, consistent with Section

VII.B.1 of the NRC Enforcement Policy (NCV 50-275/97023-02,

Example 3).

-1 2-

III. ~En ineerin

E1

Conduct of Engineering

E1.1

Inadvertent Safet

In ection Desi n Basis

an

Ins ection Sco

e

37551

The inspectors evaluated the licensee's

actions with respect to action request

0449600 which addressed

the design basis of the plant's response to an

inadvertent safety injection.

b.

Observations

and Findin s

Chapter 15.2.15 of the Updated Final Safety Analysis Report described the plant's

response

to an inadvertent safety injection event.

The sequence

of events assumed

that the positive displacement

pump (one per unit) was initially in operation.

Upon

initiation of the safety injection signal, both centrifugal charging pumps would

initiate and immediately inject into the core.

Operators would take approximately

16 minutes to diagnose the event and take action to secure the operating charging

pumps and restore normal letdown.

The pressurizer safety valves would lift and

temporarily pass water, but would seat properly without damage

in the assumed

Chapter 15 safety analysis.

However, the vendor identified that a scaling factor used in the design basis

calculations was nonconservative.

Because of this, the Diablo Canyon Power Plant

safety analysis was reviewed, and the licensee noted that damage to the pressurizer

safety valves was not prevented

by the existing analysis.

Because of the change

in

analysis parameters,

the pressurizer safety valves would lift and pass water more

than three times, but the valves were only qualified for three water lifts.

The licensee initiated an operability evaluation that contained several interim

corrective actions.

The licensee altered their normal method of operation to operate

a centrifugal charging pump for normal charging instead of the positive

displacement

pump.

This action reduced the charging assumed

in the Chapter 15

spurious safety injection analysis.

The licensee placed an operating restriction to

allow'a maximum pressurizer level of 56 percent.

In addition, the licensee revised

the inputs to the computer code for the spurious safety injection such that each

charging pump was secured sequentially,

so that the assumed flow at various times

during the event would be less.

With the positive displacement

pump secured,

the

restrictive pressurizer

level, and the revised assumptions

in the sequence

of events,

the vendor reanalyzed the spurious safety injection event.

This new analysis

revealed that the pressurizer safety valves would not pass water several times prior

to operator action to mitigate the event, and were therefore operable.

-13-

The inspectors reviewed the licensee's operability evaluation and found it to be

technically sound.

The inspectors noted that on October 24, 1997, the licensee

experienced

a spurious safety injection event.

Timely operator action mitigated this

event and prevented

pressurizer overfill as discussed

in NRC Inspection Report

50-275; 323/97019.

Therefore, the inspectors concluded that the licensee's

reanalysis and operability evaluation to be conservative.

C.

Conclusions

Engineering personnel provided a timely and technically sound response to concerns

with the design basis of the plant's response to a spurious safety injection signal.

E1.2

Technical S ecifications Inter retations

a.

Ins ection Sco

e

37551

The inspectors reviewed the licensee's Technical Specifications interpretations to

evaluate if they were consistent with.NRC requirements.

b.

Observations

and Findin s

NRC Information Notice 97-80, "Licensee Technical Specification Interpretations,"

discussed

several issues in which licensees

had Technical Specifications

interpretations that conflicted with the specific wording of the Technical

Specifications.

In December 1996, Diablo Canyon personnel

performed a review of

their Technical Specification interpretations

and identified several concerns with

these interpretations,

After identifying these concerns,

the licensee has continued

to implement these interpretations while preparingdicense

amendments

for them.

Specifically, the inspectors

had concerns with Technical Specifications

interpretations

88-01 (applicability of 25% grace period for conditional

surveillances),

89-07 (compliance with off-site power specifications), 94-08

(allowance of centrifugal charging pump usage during low temperature/over

pressure

conditions), 96-05 (actions to be taken when both undervoltage

relays are

inoperable),

and 94-07 (use of positive displacement

pump during low

temperature/overpressure

conditions).

These items are pending further NRC review to determine the validity of the

licensee's

position.

This is an unresolved item (URI 50-275;323/97023-01).

-14-

E2

Engineering Support of Facilities and Equipment

E2.1

O erabilit

Evaluation of Containment

Fan Cooler Units

CFCU with Stator to Motor

Frame Weld Cracks

Ins ection Sco

e 37551

Operability Evaluation 97-07, Revision 1, was reviewed to determine the technical

adequacy of the evaluation and the operability of the CFCU motors with cracks in

the stator compression

bars to motor frame

welds.'bservations

and Findin s

The licensee discovered cracks in two stator compression

bar to frame welds during

an inspection of a spare CFCU motor removed from Unit 1 during 1R8. Two other

spare CFCU motors, offsite for repair, had similar cracked welds.

Engineering

operability evaluation Operability Evaluation 97-07 documented

the conclusion that

the ten installed CFCUs were operable.

The CFCU motors are two speed motors, with 300 and 100 horsepower ratings for

high and low speed, respectively.

The CFCUs were normally operated

in high

speed, but switch automatically to slow speed

on a safety injection signal.

The

motor stator consisted,

in part, of hundreds of thin segmented

circular laminations.

These laminations were held together by 3/4 inch thick circular end rings.

During

construction,

a compressive force was applied to the end rings to hold the

laminations in place.

This compression force was maintained by six 25-inch long

compression

bars (cross sectional dimensions

2 inches by 1/2 inch) spaced at 60

degrees

apart on the outside circumference of the stator.

The compression

bars

were welded at each end to the end rings.

The compression

bars extended

1-3/8

inches past the end of the stator and were welded to the end frames by fillet welds.

The dimensions of these fillet welds depended

on the amount of filler weld

necessary to properly center the stator to the end frame to ensure concentricity of

the rotor to the stator.

The compression

bar at the base of the stator was also

welded to a frame bar with two additional 1-inch welds.

Diablo Canyon Units

1 and 2 have a total of thirteen CFCU motors, five in each unit

and three spares.

One spare was in the cold machine shop when the weld cracks

were originally identified.

Prior to 1R8, the other two spare CFCU motors were sent

to a vendor for wiring modifications and overhaul.

During the overhaul, several

weld cracks were identified and repaired by the vendor.

The motors were returned

and installed, but neither motor performed acceptably during testing.

The motors

made signi;icant noise and did not reach rated speed during loaded testing.

The

motors were returned to the vendor for investigation and repair.

The licensee

believed that the weld repairs changed

the orientation of the rotor to stator,

resulting in an unbalanced

magnetic pull that prevented the motors from properly

operating under load.

-15-

The visual examination and evaluation of the cracks in the CFCU motor in the

machine shop determined the cracks to be caused

by service related fatigue.

Based

on this conclusion, the cracks would form and propagate

as a result of cyclic loads

and vibration.

The greatest cyclic loads occur during starts in slow speed.

The

motors were routinely started in slow speed before heing shifted to high speed for

normal. operations.

Engineering assessment

of the loads due to vibration during

operation determined that the loads were low when compared to loads imposed

when starting the machines.

Engineering concluded that it was improbable that

normal operating loads would propagate the weld cracks.

Therefore, crack

propagation

appeared to have occurred during repetitive motor starts.

Cracks in similar welds were identified in the 1980s at another facility. The other

licensee identified the cracks when they investigated repeated thermal overload trips

of their fan cooler motors when started in slow speed.

This other licensee

determined that a significant contributor to the failures was an unbalanced

magnetic

pull which resulted from a lack of concentricity between the rotor and the stator.

The corrective actions included frame weld repair and minor motor modifications.

The other licensee's motor problems were limited.to their ten 1969 vintage motors.

Diablo Canyon personnel performed borescope

inspections of the inservice CFCU

motors which had been manufactured

in 1969 or 1970.

The vendor provided

criteria for determining whether a motor was operable.

Without a specific analysis

of a given configuration, if each compression

bar had at least one compression

bar

to frame weld intact, it would perform its function.

Using this criterion, the utility

evaluated the two 1969 inservice motors and determined

CFCU 1-5 met the vendor

criteria and CFCU 2-3 did not.

Three 1970 vintage CFCU motors were also

inspected

and met the vendor criteria. The remaining five inservice CFCU motors

were manufactured

later.

The vendor believed the two 1978 and 1979 vintage

motors had better welds.

The three late 1980s and early 1990s vintage motors had

a different frame design and less run time.

Based on this information and no history

of failures due to cracked welds in these later models, the licensee determined these

CFCU motors to be operable.

The utility performed

a specific analysis of the CFCU 2-3 motor and concluded it

was operable

based on 1) sufficient weld cross sectional area, with conservative

margins, to meet the load requirements of a slow speed motor start concurrent with

~

a seismic event; 2) the number of starts expected

before 2RS was small and crack

growth was not expected to be significant prior to 2RS; and 3) a motor inspection

was scheduled to be performed at approximately the mid-point between the last

inspection and the start of 2RS.

Additional inspections of CFCU motors of various

vintages were tentatively planned prior to 2RS.

Conclusions

The operability evaluation considered the degraded

condition, the design and

construction of the motors, the probable cause of the cracked welds, the potential

0

-16-

failure modes, the specific safety function of the CFCUs, the inherent redundancy of

needing

o'nly two of five coolers to meet the design basis, and the history of

failures, including-those identified at another facility. The operability evaluation

provided adequate justification to support the operability determination.

ES

Miscellaneous Engineering Issues (92903)

E8.'I

Closed

IFI 50-275'323 92016-04:

recirculation phase design basis.

This item

was opened

in 1992 when an inspector believed that the licensee may have had an

insufficient understanding

of design basis requirements for the recirculation phase of

emergency core cooling system operation,

This item involved five individual items,

three of which were subsequently

closed.

Due to an administrative error, this

followup item was closed before actions for the two remaining items were

reviewed.

The inspector reviewed licensee documents

and confirmed that the

licensee evaluated

and completed actions for the two remaining items.

Since 1992,

the inspectors note that the licensee has updated their design criteria memorandum

for the operation of the emergency

core cooling system.

The inspectors also note

that emergency core cooling system operation was reviewed and documented

in

NRC Inspection Reports 50-275;323/96023

and 50-275;323/97003.

Accordingly,

no additional action is required for this followup item.

R1

Radiological Protection and Chemistry Controls

R1.1

General Comments

During this inspection period, the inspectors observed radiation protection controls.

The inspectors noted that licensee personnel followed basic radiation practices such

as proper wearing of dosimetry and protective clothing.

All high radiation area

doors were locked as required, and radiation protection postings were properly

maintained.

S1

Conduct of Security and Safeguards Activities

S1.1

General Comments

71750

During routine tours, the inspectors noted that the security officers were alert at

their posts, security boundaries

were being maintained properly, and screening

processes

at the Primary Access Point were performed well. During backshift

inspections,

the inspectors noted that the protected area was properly illuminated,

especially in areas where temporary equipment was brought in.

0

-1 7-

V. Mana ement Meetin s

X1

Exit Meeting Summary

The inspectors presented

the inspection results to members of licensee management

at the

conclusion of the inspection on January

16, 1998.

The licensee acknowledged

the

findings presented.

The inspectors

asked the licensee whether any materials examined during the inspection

should be considered

proprietary.

No proprietary information was identified.

ATTACHIVlENT

SUPPLEMENTAL INFORMATION

PARTIAL LIST OF PERSONS CONTACTED

Licensee

J. L. Becker, Assistant Manager, Maintenance

M, A. Crockett, Manager, Nuclear Quality Services,

R. D. Gray, Director, Radiation Protection

T. L. Grebel, Director, Regulatory Services

D. T. Miklush, Manager, Engineering Services

J. P. Molden, Manager, Operations Services

D. R. Oatley, Manager, Maintenance

Services

R. P. Powers, Vice President and Plant Manager

L, L. WomnaC, Vice President,

Nuclear Technical Services

INSPECTION PROCEDURES

(IP) USED

IP'37551

IP 61726

IP 62707

IP 71707

IP 71750

IP 92700

IP 92901

IP 92902

IP 92903

Onsite Engineering

Surveillance Observations

Maintenance

Observation

Plant Operations

Plant Support Activities

Onsite Followup of Written Reports of Nonroutine Events at Power Reactor

Facilities

Followup - Operations

Followup - Maintenance

Followup - Engineering

0

0

0

-2-

ITEMS OPENED AND CLOSED

~O'ened

50-275;323/

97023-01

URI

Questionable

Technical Specification 'Interpretations

(Section E1,.2)

Closed

50-275/

95-006-00

LER

Loads moved over spent fuel pool with inoperable ventilation systems

(Section 08.2)

50-275/

96-009-00

LER

Auxiliary feedwater pumps inoperable due to inadvertent blockage of

a ventilation flow path (Section 08.3)

50-275/

96-002-00

LER

50-275/

96-004-00

LER

50-275/

85-043-00

LER

50-323/

96009-01

VIO

50-275/

9601 9-02

VIO

50-275;323/

9201 6-04

IFI

Technical Specification 3.6.1.1 not met due to personnel

error

(Section M8.1)

Technical Specification 3.3.3.5 not met due to personnel error

(Section M8.2)

Technical Specification 3.3.2 was not met due to an inadequate

procedure

(Section M8.3)

O.

Loads moved over spent fuel pool with inoperable ventilation systems

(Section 08.2)

Failure to report off clearance

prior to removing ground buggies

(Section 08.1)

Recirculation phase design basis (Section E8.1)

0 ened and Closed

50-275/

97023-01

50-275/

97023-02

NCV

Inoperable auxiliary feed pumps due to blocked ventilation flow path

(Section 08.3)

NCV

Three examples of missed surveillance tests (Section M8)