ML15261A314

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Insp Repts 50-269/93-25,50-270/93-25 & 50-287/93-25 on 931101-1214.Violations & Deviations Noted.Major Areas Inspected:Svc Water Sys Operational Performance Insp
ML15261A314
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 02/10/1994
From: Peebles T, Rogers W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML15261A311 List:
References
50-269-93-25, 50-270-93-25, 50-287-93-25, GL-89-13, NUDOCS 9402230266
Download: ML15261A314 (54)


See also: IR 05000269/1993025

Text

pj% REG&

UNITED STATES

0G

NUCLEAR REGULATORY COMMISSION

A

REGIONlII

o

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

Report Nos.:

50-269/93-25, 50-270/93-25 and 50-287/93-25

Licensee:

Duke Power Company

422 South Church Street

Charlotte, NC 28242

Docket Nos.:

50-269, 50-270, and 50-287

License Nos.:

DPR-38, DPR-47,

and DPR-55

Facility Name:

Oconee 1, 2 and 3

Inspection Conducted: November 1 through December 14, 1993

Inspector:

r Walter G. Rogers, Team Leader

Date Signed

Accompanying Personnel:

L. Mellen

C. Rapp

L. King

K. Kavanaugh (Intern)

D. Tamai (Intern)

P. Holmes-Ray

Approved by:

homas A. Peebles, Chief

Date Signed

perational Programs Section

e- Operations Branch

Division of Reactor Safety

SUMMARY

This routine, announced inspection was conducted in the areas of Service Water

System Operational Performance Inspection (SWSOPI) on November 1 through

December 14, 1993, in accordance with NRC Temporary Instruction 2515/118.

RESULTS

General Weaknesses:

The NRC Temporary Instruction for Service Water Inspections, SIMS item

2515/118, was not closed due 'to licensee inadequacies in response to GL 89-13. Design control measures contained numerous weaknesses.

Unvalidated and nonconservative assumptions were used in various

calculations. Calculations or analyses did not exist for some SWS

operating modes.

Engineering analyses of some conditions were

9402230266 940211

PDR ADOCK 05000269

a

PDR

2

inadequate. Vague criteria had been established for updating

calculations. The testing program had but omitted critical functions of

some systems and equipment. The procedural guidance for some abnormal

situations was weak. The safety classification system had numerous

omissions. Resolution to self-assessment findings were sometimes

untimely and occasionally inadequate.

General Strengths:

The SWSs were in good material condition. The design review portion of

the licensee's self assessment was thorough and comprehensive for the

system reviewed.

Instrument calibration procedures contained detailed

and complete descriptions of the instrument's function. The corrosion

monitoring program, though of limited scope, was excellent. The DBD

concept and the associated testing acceptance criteria were good

initiatives.

Findings

LPSW System - For some low probability situations required by the

facility's license, the system would be incapable of performing its-,

safety function. For example, RBCU cooling coil leak repair material

had not been qualified for accident conditions; failure of the material

would affect containment integrity. A fairly complete hydraulic

computer model had been developed, but inadequate controls existed for

maintaining the hydraulic model valid. Significant material condition

improvements had been accomplished (replacement of the unreliable

radiation monitoring system) and others were planned (replacement of all

RBCUs). Extensive analysis/calculations existed on which the system

design was based. However, analyses dealing with LPSW NPSH and RBCU

waterhammer were inadequate. Also, the RBCU performance evaluation

process contained two questionable inputs.

CCW System - Corrective actions to SITA findings associated with the

ECCW subsystem had been untimely. Portions of the CCW system necessary

to provide flow to the LPSW system were not properly classified as

safety-related. The situation had been recognized by the licensee, and

adequate corrective actions were being implemented. No analyses existed

to support Oconee's capability to withstand failure of the Keowee

Dam/loss of inventory of the Lake Keowee. Also, the procedures for this

scenario contained weaknesses. The test procedure and heat transfer

calculations for the ECCW subsystem were inadequate. Fortunately, a

large safety margin existed in the actual system's performance.

HPSW System - The system was not classified, constructed, tested, or

maintained commensurate with its importance to safety. The licensee's

engineering organization recognized this deficiency. However,

communication to the rest of the organization had been untimely. Also,

some of the corrective actions taken by the licensee in response to this

deficiency were weak.

3

SSF - The SSF would not remain operational following a failure of the

Jocassee Dam. Therefore, no system was available to provide decay heat

removal of the three units in this situation. Also, the decay heat

removal function of the SSF had not been adequately confirmed. The

minimum flow requirements to the steam generators were nonconservative.

Numerous calculations had not been updated following facility

modifications affecting the calculations. The periodic testing program

elements did not add up to an integrated test of the SWS systems.

Air

entrapment affecting ASW pump performance could not be identified during

periodic pump testing due to a procedure deficiency. Finally, certain

aspects of the licensee's GL actions had not been performed.

ASW System - The system was marginal in its capabilities and did not

contain flow instrumentation or provide the operators the ability to

control plant conditions from the control room. Testing of the system

failed to provide full assurance that the personnel could perform

necessary tasks within the requisite time constraints. The testing of

specific components in the system was inadequate, but the licensee had

recognized the deficiencies and was taking timely corrective actions.

Calculations for NPSH and pump minimum flow protection lacked rigor.

Keowee - The mechanical systems were very reliable. Keowee had been

excluded from the licensee's GL response. Corrective actions to

establish all aspects of the quality assurance program at Keowee had

some minor weaknesses in quality of implementation and full integration.

Also, some minor quality assurance program deficiencies were present.

The calibration program contained some weaknesses including not

verifying the annunciator panels alarm at the proper setpoint.

Four cited violations, two non-cited violations, two deviations, one

unresolved item, and six inspector follow-up items were identified.

The following items are included as attachments to this inspection report:

APPENDIX A Persons Contacted

APPENDIX B Generic Letter 89-13 Action Items

APPENDIX C Acronyms and Abbreviations

REPORT DETAILS

1. Inspection Objectives

Numerous problems identified at various operating plants in the United

States have called into question the ability of SWSs to perform their

design function. These problems have included inadequate heat removal

capability, biofouling, silting, single failure concerns, erosion,

corrosion, insufficient original design margin, lapses in configuration

control or improper 10 CFR 50.59 safety evaluations, and inadequate

testing. NRC management concluded that an in-depth examination of SWSs

was warranted based on these problems.

The team focused on the mechanical design, operational control,

maintenance, and surveillance of the SWS and evaluated aspects of the

quality assurance and corrective action programs related to the SWS. The

inspection's primary objectives were to:

Assess SWS performance through an in-depth review of the system's

mechanical functional design and thermal-hydraulic performance

including the content and implementation of SWS operating,

maintenance, and surveillance procedures, and operator training on the

SWS,

Verify that SWS functional design and operational controls could meet

the thermal and hydraulic performance requirements, and that SWS

components were operated in a manner consistent with their design

bases,

Assess the licensee's planned and completed actions in response to

Generic Letter 89-13, "Service Water System Problems Affecting Safety

Related Equipment," July 1989, and

Assess SWS unavailability resulting from planned maintenance,

surveillance, and component failures.

The specific areas reviewed are described in paragraph 2 of this report.

The observations and concerns identified are described in paragraphs 3

through 10 of this report. Personnel contacted and those who attended the

exit on December 14, 1993, are identified in Appendix A.

2. Inspection Areas of the SWSs Associated with Oconee

The SWSs at Oconee encompassed numerous systems. These were the LPSW;

HPSW; ASW; CCW (including the ECCW subsystem); the EDG cooling, HVAC

cooling, steam generator cooling, and submersible pump subsystems of the

SSF; and most of the mechanical systems of the Keowee hydroelectric

station.

The team reviewed the mechanical design of each SWS, including the design

bases, functional requirements, design assumptions, calculations, boundary

conditions, analyses and models to determine if the design met licensing

commitments and regulatory requirements. Each SWS's capability to meet

the thermal and hydraulic performance specifications during accident and

Report Details

2

abnormal conditions was reviewed. The design features associated with the

loss of the Jocassee and Keowee Dam were evaluated. Single and common

mode failure vulnerabilities, selected modifications and proper reflection

of SWS design in plant operations, testing, and maintenance procedures

were reviewed. The team reviewed maintenance history on selected

equipment, maintenance procedures, completed work packages, preventive

maintenance schedules, preventive maintenance procedures, and associated

LERs. The availability records of the LPSW system for the past two years

was compared to the licensee's PRA submittal.

Plant walkdowns were

conducted on all SWSs to assess present operating configurations,

conformance to design documents, housekeeping and material conditions.

Normal, abnormal and emergency operating procedures were reviewed for

adequacy. Simulator scenarios involving the LPSW system were evaluated.

The team reviewed preoperational test procedures, surveillance procedures,

and the IST program implementation to determine if sufficient testing had

been conducted to confirm system design requirements and system

operability. Also reviewed were the licensee's procedures, controls, and

other activities associated with the calibration of instrumentation in the

SWSs.

The team reviewed the licensee's self-assessment of the LPSW system

and select corrective action documents associated with the SWSs. The

minutes of off-site committee meetings were reviewed for.conformance to

Technical Specification requirements. Also, the team evaluated the

adequacy of the licensee's GL 89-13 actions associated with all the SWSs.

3. Generic Letter 89-13 Implementation

The NRC issued GL 89-13, "Service Water System Problems Affecting Safety

Related Equipment," requesting licensees to take certain actions related

to their SWS. These actions included establishing biofouling surveillance

and control techniques, monitoring safety-related heat exchanger

performance, establishing a routine inspection and maintenance program,

reviewing the design to assure intended safety functions could be

accomplished, and training personnel in the operation, maintenance, and

testing of the SWS.

The licensee's docketed responses to the GL of January 26, 1990, and

May 31, 1990, were broad in nature and not specific to each system

addressed. Also, the licensee's response indicated the GL actions had

been performed without taking exceptions.

However, the licensee's GL actions almost exclusively focused upon the

LPSW system and its support systems. The licensee's actions in response

to GL 89-13 did not address all the applicable GL systems. The SWS

associated with the Keowee hydroelectric station was not considered. A

number of GL actions were not considered for the ASW and the SWS portion

of the SSF. Also, a number of GL actions were not performed by the

licensee for the HPSW system due to the classification of the system as

nonsafety-related. Failure to apply the GL actions to all the applicable

systems is Deviation 50-269, 270, 287/93-25-01, "Failure to Adequately

Perform SWS GL Actions."

Report Details

3

The licensee had performed extensive corrective actions to the LPSW

system, but one LPSW design deficiency identified during self-assessment

activities was riot properly rectified. Also, corrective actions

associated with the support functions provided by the CCW system had not

been performed in a timely manner and/or did not fully address the

deficiencies identified.

Heat exchanger performance monitoring was adequate for the LPI coolers and

the smaller LPSW system coolers. The RBCU performance monitoring had

established relative changes in the fouling factor between monitoring

intervals but had not determined the true fouling factor. Also, some of

the inputs associated with RBCU performance monitoring were questionabl,

in that the licensee was continuing to improve the hydraulic model for

LPSW. See Appendix B for details on each GL 89-13 Action Item.

4. Low Pressure Service Water System

The LPSW system provided cooling to the RBCUs, LPI coolers, the motor and

turbine driven EFW pump coolers, HPI pump motor coolers, the control room

chilled water system, numerous room coolers, and nonsafety related turbine

building loads. Units 1 and 2 shared three 15,000 gpm pumps with one pump

capable of being powered from two separate safety related busses. The

Unit 3 LPSW system had two 15,000 gpm pumps. The LPSW pumps took a

suction from the 42" CCW discharge header within the turbine building.

The Unit 1/2 LPSW pumps discharged into a common header that split into

two supply lines; one supply line for each unit. The unit supply lines

further divided into two separate headers supplying the two trains of

safety related equipment. The two equipment supply lines then

interconnected into a common line which entered containment. This common

line then split into three parallel lines, each line supplying one RBCU.

These three RBCU supply lines then reconnected into one line on the

discharge side of the RBCUs before exiting containment. Also, branching

from the common discharge header was a supply line to the turbine building

loads.

The turbine building supply line then'split to provide cooling to

each unit's turbine building equipment. The Unit 3 RBCU and turbine

building cooling arrangement was similar. A normally closed crosstie line

allowed either LPSW system to supply the discharge header of the other

LPSW system.

Inspection findings related to the LPSW system were:

a. Turbine Building Isolation

(1) Design

The licensee's design for isolating the nonseismic turbine

building line from the seismic portion of the LPSW system was

inadequate. A single, motor operated butterfly valve was

provided, even though the two LPSW trains were designed and

operated as one interconnected system. The isolation valve for

Report Details

4

Units 1/2 was LPSW-139, and LPSW-45 for Unit 3. The valves did

not have an auto-closure feature, but could be electrically

closed by operator action from a station just outside the control

room. The isolation valves had not been originally specified as

seismic but were seismically qualified as a resolution to a 1987

SITA finding on the LPSW system.

The licensee had performed calculations to determine the effect

an earthquake would have on the LPSW systems. In the case of a

nonseismically supported turbine building line failure without

turbine building isolation, the calculation indicated the LPSW

system would not be able to supply adequate cooling to the

required safety related loads.

FSAR Section 9.2.2.2.3 stated in part, "The LPSW system provides

sufficient flow to the Low Pressure Injection coolers and Reactor

Building Cooling Units to ensure sufficient heat transfer

capability following a design basis accident and a single active

failure. The worst case design basis accident involves a

LOCA/loss of offsite power with seismic event."

The licensee stated that failure of a seismic/non-seismic

interface valve was outside the licensing basis for the facility.

The team disagreed. This is Unresolved Item 50-269, 270, 287/93

25-02, "Turbine Building Isolation Single Failure

Vulnerabilities."

(2) Testing

The isolation valves had not been VOTES tested in response to GL 89-13, "Safety Related Motor Operated Valve Testing and

Surveillance."

LPSW-45 was scheduled for VOTES testing at the

next refueling outage. LPSW-139 was scheduled for VOTES testing

at the next outage of both Units 1 and 2. In response to the

team's request for design calculations supporting the closing

capability of these valves, the licensee performed calculation

OSC-6019, Valve LPSW-139 and 3LPSW-45, "Closure Against Maximum

Delta P," indicating that adequate closing thrust could be

developed.

Stroke testing of the valves had been limited. LPSW-45 was

stroke tested once per refueling outage. Due to operating

constraints associated with closing LPSW-139, it had been stroke

tested only once since initial operation.

b. LPSW Pump NPSH Considerations

Calculations extrapolating system testing results identified several

configurations involving loss of instrument air where LPSW flow demand

was greater than design. The most severe configuration was

Report Details

5

simultaneous operation of both LPI coolers on a shutdown unit and a

LOCA on the other unit with the LOCA unit's MTOTC temperature control

valve bypassed. For this case, there was insufficient NPSH for the

excessive LPSW flow demand causing significant cavitation of the LPSW

pumps. The licensee established procedural controls to throttle LPSW

flow within 30 minutes through operator actions, thereby eliminating

the cavitation. The inadequate NPSH condition was evaluated by the

licensee and considered acceptable.

(1) The licensee's NPSH acceptability evaluation was based upon

accepting the manufacturer's best judgement that no significant

pump degradation would occur during and following the inadequate

NPSH condition. Neither the licensee nor the pump manufacturer

performed any testing validating this judgement. Also, the pump

manufacturer did not warrant the LPSW pumps for operation with

insufficient NPSH. Therefore, the licensee failed to adequately

validate this critical design assumption. 10 CFR 50, Appendix B,

Criterion III, "Design Control," requires that adequate measures

be established for the selection of equipment. Also, as

committed through Duke Power Company Topical Report 1-A, Table

17.0-1; ANSI 45.2.11-1974, "Quality Assurance Requirements for

the Design of Nuclear Power Plants," requires NPSH be considered

as a design input in Section 3.2.11.

This is considered an

example of Violation 50-269, 270, 287/93-25-03A, "Failure to

Perform Adequate Calculations and Evaluations to Support Facility

Design."

(2) One of the operator actions to reduce flow demand within 30

minutes was throttling the LPI cooler isolation valves until

reaching 3000 gpm. The cooler isolation valves were gate valves

and, generically, not used for throttling. The licensee had

evaluated and tested these valves for throttling flow and

determined the valves could be throttled. However, after

throttling, the valves may not go full open or closed due to

internal damage suffered while throttled. This could result in

the inability to isolate a leaking LPI cooler subsequent to the

throttling activities.

c. The Hydraulic Model

(1) The licensee's hydraulic computer model for predicting LPSW

system response during an accident used the manufacturer's pump

curves. The manufacturer's pump curves did not include pump

degradation. Quarterly inservice pump testing allowed for up to

10 percent pump degradation without declaring the pump

inoperable. There were no procedural controls to evaluate the

inservice pump test results against the hydraulic model's flow

inputs. Although the situation was not identified during the

inspection, an acceptable inservice pump test could invalidate

the LPSW pump flow inputs to the hydraulic computer model.

Report Details

6

Contrary to the requirements of 10 CFR 50, Appendix B, Criterion

III, "Design Control," the licensee failed to provide the

adequate procedural controls to ensure the LPSW hydraulic model

was not invalidated. This is an example of Violation, 50-269,

270, 287/93-25-038, "Failure to Perform Adequate Calculations and

Evaluations to Support Facility Design."

(2) The manufacturer's pump curve indicated the possibility of

deadheading a degraded pump when the LPSW pumps were operating in

parallel. Trending of the one point flow/pressure check used in

the IST program was not the most reliable method of detecting

pump degradation. The development of an individual pump curve

would more accurately predict this condition. However, the

current testing method was consistent with regulatory

requirements.

(3) In 1992, the licensee reviewed Unit 1 and 2 hydraulic computer

model results and determined a waterhammer would occur during a

design basis LOCA with a single failure. The hydraulic model

predicted a LPSW pressure of -13.5 psig downstream of the RBCU

discharge throttle valves. Containment temperature would exceed

200*F in response to the design basis LOCA. The combination of

the low pressure (-13.5 psig) and the high temperature (200'F)

would cause the LPSW water to flash to steam. Upon condensation

of the steam, a waterhammer would ensue. Under condition adverse

to quality report PIP 92-454, the licensee evaluated the effects

the waterhammer would have on LPSW flow within the piping and the

reduction in RBCU cooling in calculation OSC-4922, "LPSW Woods

Model Flowrate Correction through RBCU's Due to Cavitation,"

issued September 25, 1992. The licensee did not evaluate the

effects the waterhammer would have on the structural integrity of

the RBCUs and the discharge piping. 10 CFR 50, Appendix B,

Criterion XVI, "Corrective Actions," requires conditions adverse

to quality to be promptly identified and corrected. This is

considered an example of violation 50-269, 270, 287/93-25-04A,

"Inadequate Evaluation of Conditions Adverse to Quality by

Engineering."

d. RBCU Operability Determination

A combination of LPSW flow test data and computer modeling of RBCU air

flow were used to determine if the RBCUs had adequate accident

condition heat removal capability. There were two questionable inputs

used in that determination as follows:

(1) Accuracy of the installed orifice used to measure LPSW flow

A reduction in the diameter of the piping in the area of the

orifice would result in higher indicated LPSW flow than was

actually occurring. Documentation and photographs showed fouling

Report Details

7

had occurred at various points within the LPSW piping. Anomalous

results in previous flow testing, though possibly due to other

reasons, could be explained by the flow instrumentation reading

high. The licensee was aware of the potential problem and

planned to replace the RBCUs and associated piping, including the

section containing the flow orifice, at the next refueling outage

for each unit.

(2) Validity of the RBCU non-uniform air flow distribution predicted

by the computer modeling

The calculation of the air side fouling factor was highly

sensitive to variations in the air flow distribution. The

computer code had been benchmarked by a vendor. However, an

airflow test performed in 1987, indicated airflow was

substantially less than expected. When questioned about the

results, the licensee stated this test was invalid due to

significant air side fouling. Further testing was not conducted.

These two concerns placed RBCU results in question. Further licensee

actions to determine the accuracy of these two inputs into AN RBCU

operability determination is considered an Inspector Follow-up Item

50-269, 270, 287/93-25-05, "Additional Validation of RBCU Evaluation

Inputs."

Also, a detailed discussion of RBCU operability

determination is contained in Appendix B, section II.

e. Use of Belzona for RBCU Leak Repair

The licensee had used Belzona to repair various plant components

including the pressure retaining braze joints on the RBCUs. The

commercial grade evaluation, CGD 2021.01-01-0001, specifically

addressed the use of Belzona as a pressure retaining material for

"pinhole" leak repairs on the Unit 2 RBCU coils. While the licensee's

calculation found that the shear stress was acceptable; the licensee

failed to evaluate or obtain test data to show that the RBCU repairs

would withstand accident conditions.

Failure of the Belzona presently

installed in Unit 2 coincident with a LOCA would significantly

increase containment leakage.

10 CFR 50, Appendix B, Criterion III,

"Design Control," requires adequate suitability of application of

materials reviews be performed. This is considered an example of

Violation 50-269, 270, 287/93-25-03C, "Failure to Perform Adequate

Calculations and Evaluations to Support Facility Design."

f. Simulator Observations

(1) During a LOOP/LOCA with failure of one LPSW pump on the shared

Unit 1/2 system, the operator stopped one of the two operating

LPSW pumps when no pump amperage was indicated. Redundant,

independent instrumentation was not used prior to stopping the

pump and was considered a performance weakness. Although

Report Details

8

expected and consistent with the facility's design, LPSW pump

suction valve position indication was lost.

Indication was

powered from a nonsafety related electrical bus which de

energizes in response to the LOOP. These valves were normally

aligned open and do not receive an ESF signal.

The lack of

indication contributed to the operator's decision to stop the

pump.

(2) With one operating LPSW pump supplying both units, the LPI cooler

flows required by the emergency procedure could not be achieved.

None of the licensee's procedures were applicable to this

situation. The operators used their judgement and secured LPSW

flow to the LPI coolers, isolated cooling to the control room,

and isolated numerous nonessential loads. After transferring LPI

pump suction to the containment sump due to depletion of the

BWST, the LPI coolers were returned to service at flows less than

required by the emergency procedure.

The lack of specific procedural direction was due to a deficiency

within the abnormal procedure for total loss of LPSW. The entry

condition for using this procedure was no LPSW pump operating;

instead of inadequate LPSW flow. The licensee acknowledged this

deficiency. Actions to improve operator response to inadequate

LPSW flow is considered part of Inspector Follow-up Item

50-269,270, 287/93-25-06A, "Actions to Improve Operator Responses

to Abnormal Events."

(3) After the simulator demonstration, the ramifications of reduced

LPI flow and the bases of the procedurally required 3000 gpm LPI

cooler flow was discussed. This parameter directly involved

maintaining containment temperature less than equipment

environmental qualification temperature limits. Licensee

responses were focused exclusively on reactor core cooling. The

3000 gpm bases for LPI cooler flow was not fully understood by

the individuals. This was due to the limited training on

containment temperature concerns during an accident. The

licensee responded that containment temperature ramifications

would be the responsibility of the Technical Support Center.

This is considered a training weakness.

(4) The simulator was certified. However, there was no simulation of

the HPI and LPI pump motor coolers, no deviation in LPSW flow to

the RBCUs in response to the ESF actuation, and no simulation of

the Unit 3 LPSW system crosstie.

Report Details

9

g. SITA Actions

In 1987, the licensee conducted a technical audit of the LPSW system.

The audit was thorough with a substantial number of findings. Some of

the corrective actions directly associated with the LPSW system were

adequately dispositioned. Examples included the replacement of the

unreliable radiation monitoring system for effluents from the LPSW

system, development of a hydraulic computer model, and the generation

of a substantial number of calculations to support LPSW design.

However, concerns by the licensee associated with some of the

corrective action resolutions, especially dealing with support

systems, prompted an October-November 1992 review of the SITA process

and revisiting a number of these outstanding issues. Subsequently, a

SWS Steering Committee was formed and charged with resolution of all

SWS issues.

The team concurred with the licensee's assessment that there had been

untimely progress of some critical SITA issues prior to the Fall,

1992.

The SITA process review in the Fall, 1992, was a good

initiative. Also, the resulting SWS Steering Committee had a number

of positive aspects including centralization of the issues and the

ability to focus the diverse sections of the Oconee organization on

resolution of a particular issue. However, resolution of some of the

outstanding issues was inadequately addressed. Examples included the

LPSW turbine building isolation, and HPSW piping seismic capability.

h. System Availability

Recent syst=m availability data compared favorably with the

availability assumed in the IPE report. Also, the material condition

of the LPSW system was good except for fouling of small diameter

piping. Recent machinery history records indicated the majority of

the repetitive corrective maintenance focused on unplugging fouled

instrument impulse lines. Also, flow testing of the Unit 3 HPI pump

motor cooler, the Unit 1 LPSW A pump's cooling line, and the TDEFW

pump cooling lines indicated fouling resulting in stainless steel

piping replacements in those areas.

5. Circulating Cooling Water'System

The CCW system was common to all three units and took suction from the

Lake Keowee intake canal.

Twelve pumps (four per unit) supplied a common

cross-connected 42-inch discharge header from which numerous other SWSs

took suction. From this header, cooling water passed through the three

condensers. Upon leaving the condensers, the water discharges through six

lines (two per unit) and returns to Lake Keowee upstream of the intake

canal.

Report Details

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A subsystem of CCW was the ECCW system. If the CCW pumps lost power ECCW

actuated establishing siphon or gravity flow from the intake canal to the

42-inch header and through the condenser sections. Emergency condenser

discharge lines connect the condensers with the Keowee hydroelectric

station's tailrace and due to elevation differences. This was

gravity/siphon flow operated. Prior to entering the tailrace all the

discharge lines connected into one line. ECCW actuation involved the

automatic closure of the condensers' normal outlet valves, opening of the

condensers' emergency outlet valves and opening emergency discharge valve

to the Keowee tailrace, CCW-8, located in the common discharge piping.

The high points of the ECCW piping were connected to a vacuum priming

system which would remove air entrapped within the system that could

impede siphon operation. The licensee considered CCW supplying the LPSW

pumps as the first siphon and CCW passing through the condensers as the

second siphon.

The CCW system performed two distinct safety functions during the

LOCA/LOOP event:

First, it provided a suction source for other systems

including the safety-related LPSW system, and second it provided cooling

water to the condenser to remove decay heat in the emergency condenser

cooling water (ECCW) mode. The CCW pumps contributed to these safety

functions in two ways:

First, when power is lost and they are not

operating, they provided a siphon conduit from the intake canal to the CCW

piping from which the LPSW takes suction, and to the condenser for the

ECCW system. Second, at the time when the pumps can be restarted (up to

1/2 hours per emergency procedures), they continue to provide water for

these same functions. Since dissolved air will tend to come out of

solution when the system is in the siphon mode, at least one of the CCW

pumps must be operated after power is restored in order for the water to

continue to be supplied to the CCW piping.

Within the intake canal is an underwater dam which can trap approximately

67,000,000 gallons of water if Lake Keowee were to fall below the 770-foot

level.

With the CCW pumps operating the system is capable of

recirculating water from this impounded area, through the condensers,

through the condenser emergency discharge lines and through normally

closed valve, CCW-9, which discharges into the intake canal.

Findings associated with the CCW system were:

a. The Siphons

(1) The 1987 SITA identified numerous support systems associated with

the first siphon which did not meet safety related standards such

as the non-seismically qualified vacuum priming system. The

original SITA response did not refute the finding, but considered

such requirements as outside the licensing basis of the facility.

Eventually, the safety related aspects of these support systems

were evaluated in a design study. Through a combination of the

design study and a SWS steering committee the vacuum priming

Report Details

11

issue was addressed by isolating the vacuum priming system in the

Fall, 1993. Outgassing of air was addressed by establishing

minimum CCW pump combinations for particular Lake Keowee levels.

Licensee actions on this matter were untimely. Another support

system, HPSW, for the first siphon is discussed in section 6.

(2) The CCW pump components necessary to support siphon operation to

the LPSW system (the first siphon) performed a safety related

function but, were not classified as safety related. For the

first siphon to operate, the physical interface between the pump

casing and the CCW piping must be leaktight, and the pump

mounting/structural supports must be capable of withstanding an

earthquake without allowing air inleakage. Examples of the

effects of the improper classification were as follows:

(a) Following failure of an ECCW flow test the licensee

determined the cause of the test failure to be air inleakage

between the pump casing and the CCW piping. In response the

licensee issued OE # 4072 dated 6/3/91 which authorized

installation of a rubber seal at this interface. Though the

design change appeared technically adequate, it was

designated as nonsafety related.

(b) During the inspection period, the overhaul/repair of the 2B

CCW pump was being performed using nonsafety related

procedures.

(c) Whenever a CCW pump was disassembled, as with the 2B pump,

the pump casing seal was disturbed. The subsequent post

maintenance test to confirm leak tightness was performed

without written procedural direction. Following discussions

w'th the licensee the test method appeared adequate but, the

conditions for testing, the instrumentation, the acceptance

criteria, etc. were not being appropriately controlled.

Independently, the licensee recognized the error and was

classifying the components as safety related in the most current

draft revision to the Quality Standards Manual. The failure to

properly classify the components is considered Violation 50-269,

270, 287/93-25-07, "Inadequate Classification of Siphon Support

Equipment for LPSW Supply."

However, based upon the corrective

actions in progress, the licensee's self identification of the

matter, no similar violations associated with the

misclassification of the first siphon's support equipment, the

lack of willfulness, and the nonescalated enforcement nature of

the violation, this is considered a non-cited violation

authorized under 10 CFR 2, Appendix C, Section VII.B.2.

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12

(3) The licensee did not consider the equipment associated with the

second siphon as safety-related. Therefore, some of the

equipment associated with the condenser cooling mode did not meet

safety-related design requirements.

The vacuum priming support system was not seismically supported.

A number of valves were not powered from safety-related sources

including some of the condenser emergency discharge valves,

midpoint vent valves, and the emergency discharge valve to the

Keowee tailrace.

Also, the single discharge valve to the Keowee tailrace was not

seismically protected. This valve was located in a concrete and

steel structure at elevation 730 feet. The top of this structure

was covered with nonrestrained metal deck plates. In a seismic

event, the plates could fall damaging the valve or the associated

electrical cables below.

Unresolved Item, 269,270, 287/93-13-03, "ECCW System Design and

Testing," had already been established on ascertaining the

licensing basis of the ECCW system, including the condenser

cooling mode. Therefore, the design aspects of the condenser

cooling mode discussed above have been encompassed by this

unresolved item. Resolution of this unresolved issue is

contingent upon further NRC review.

(4) Nonconservatisms existed within the calculations supporting ECCW

design and testing. Examples included:

(a) Calculation OSC-2349, "CCW Intake Piping Degassing in the

ECCW Mode", Rev 1, May 21, 1990, was performed to show that

the CCW system had the capability of providing the required

flow rate even with air inleakage and outgassing of

dissolved air from the water, both of which would tend to

break the siphon. The calculation also provided the

acceptance criteria for the intake piping water level for

the "Emergency CCW System Flow Test," PT/1/A/0261/07, and

the equivalent performance tests for Units 2 and 3.

The following discrepancies and nonconservatisms existed in

this calculation:

The maximum flowrate analyzed was 30,000 gpm. However,

for the LOOP case, the maximum flowrate may include the

maximum tailrace flow through the condenser and the

CCW-8 emergency discharge valve (in the range of 30,000

gpm), plus the flows to the LPSW pumps (design flow of

15,000 gpm per pump, 5 pumps). The various LPSW pump

combinations had not been analyzed, but initial

evaluation indicated that as many as four pumps could

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13

be operating. Therefore, the actual flows could be

significantly higher than what was analyzed, producing

more outgassing due to the higher mass flow rate.

Additionally, higher flow would require a higher

minimum level in the piping to overcome the increased

flow resistance.

The atmospheric pressure used was 14.7 psia. Per

"Atmospheric Pressure for Design Calculations," S. L.

Nader, File OS-3C, 7/23/87, the correct atmospheric

pressure for Oconee was 14.0 psia.

Conservatisms in the calculation and differences from the

actual operating configuration which would tend to offset

the non-conservatisms were as follows:

The calculation assumed an outgassing rate of 100

percent. The actual rate would be less.

Actual testing was done on one unit at a time with four

CCW pump flow paths open. The calculation assumed only

one open pump flow path.

The duration of the analyzed SBO event was longer than

the LOOP event (4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> versus 1.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />).

It was not clear which will dominate, the conservatisms or

the non-conservatisms, without rigorous re-performance of

the analysis. Failure to reconcile the competing

assumptions compromised the calculation on which the

adequacy of the ECCW design requirements and test acceptance

criteria were based in part.

(b) Calculation OSC-2346, "ECCW System Performance Evaluation,"

Rev 3, February 17, 1993, was generated to show that the

condenser had the capacity to transfer the required decay

heat without exceeding the condenser pressure limitations or

causing flashing in the CCW piping which could cause loss of

the siphon. This calculation formed the basis for the

acceptance criteria of the Technical Specification required

system flow test.

(1) The methodology used to derive the heat transfer

capability of the siphon/condensers was nonconservative

as follows:

The calculation did not account for the potential

for outgassing of the CCW which would tend to

decrease the heat transfer capability of the

condenser. Such outgassing would be driven by the

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14

decrease in pressure in the CCW system due to the

siphon and by the increase in temperature of the

CCW as it passes through the condenser tubes.

The atmospheric pressure used in the calculation

was 14.7 psia. Per "Atmospheric Pressure for

Design Calculations," S. L. Nader, File OS-3C,

July 23, 1987, the correct atmospheric pressure

for Oconee was 14.0 psia.

The calculation did not account for the decrease

in heat transfer area as a result of condenser

tubes that were presently plugged and may be

plugged in the future.

The calculation did not account for the decrease

in heat transfer area due to plugging of the tubes

by the Amertap balls. The balls were continuously

recirculated through the condensers for tube

cleaning during normal operation. Due to the very

low differential pressure across the condenser

during siphon operation, the balls would stick

inside the tubes.

(2) The calculation did not address, as one of its

acceptance criteria, the requirement that the condenser

capacity in the ECCW mode should be such that the main

steam relief valves would not be open except in the

initial pressure spike transient. This criteria should

have been included to show that the system could

perform one of its primary functions, minimizing the

release of radioactivity and conserving condensate

inventory by condensing steam in the condenser rather

than exhausting it to the environment through the

relief .valves. Although the calculation was deficient

in this regard, the licensee was subsequently able to

demonstrate this capability.

(3) The calculation derived a minimum initial flow rate of

4,500 gpm to each unit's condenser to meet the heat

transfer requirements. Flow through the three

condensers was assumed to be equally split. Upon this

assumption, acceptance criteria for the Technical

Specification required flow test was derived. However,

the unit specific flow paths (the piping from the

condenser waterbox outlets to the common discharge

line) were different in length and configuration.

Also, there was not a flow analysis demonstrating the

equal flow split. Therefore, the assumed equal flow

distribution had not been validated.

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15

10 CFR 50, Appendix B, Criterion III, "Design Control," requires

that measures shall be established to assure that design bases

are correctly translated into design documents and to verify the

adequacy of design. Contrary to this requirement, the licensee

did not adequately translate the requirements for the ECCW system

into the analyses and test acceptance criteria which demonstrated

the system's capability to meet these requirements. This is an

example of Violation 50-269, 270, 287/93-25-03D, "Failure to

Perform Adequate Calculations and Evaluations to Support Facility

Design."

(5) ECCW Test Procedure

Procedure PT/1/A/0261/07, change 8, August 8, 1991, "Emergency

CCW System Flow Test," was the periodic Technical Specification

required test of the ECCW system flow capability. The flowrate

of the siphon was determined by measuring the distance between

the exit nozzle of the ECCW piping and the middle of the flume's

impact point with the tailrace. There were distance markings at

two feet increments painted on the tailrace for taking this

measurement.

Through licensee interviews, the probable width of the flume at

the point of impact was approximately three feet, and the center

of the flume was estimated to the nearest foot. Therefore,

determination of the flume's impact point entailed an error of as

much as + one foot, which represented an error of approximately +

2,000 gpm in the acceptance criteria. This potential error was

not accounted for in the test acceptance criteria. 10 CFR 50,

Appendix B, Criterion XI, Test Control, requires that, "Test'

procedures shall include provisions for assuring that.. .adequate

test instrumentation is available and used..."

This is

considered an example of Violation 50-269, 270, 287/93-25-08A,

"Inadequate Testing Methods for Testing SWS Equipment."

(6) Although the ECCW calculations and the test procedure were

inadequate, the most current test results of ECCW flow appeared

to support system operability. This was due to:

(a) The current test procedure verifying the ECCW mode

capability, PT/1/A/0261/07, change 8, August 8, 1991, was

based on the more conservative analysis in Rev. 2 of the

calculation which required an initial flow rate of 6,000 gpm

per unit instead of 4,500 gpm per unit. This procedure's

acceptance criteria started at 18,000 gpm flow and decreased

with time based on an implied assumption that flow through

the three unit condensers would be evenly distributed.

(b) Total ECCW flow was approximately 30,000 gpm.

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(7)

Under Minor Modification OE # 5514 dated September 16, 1993, the

licensee deleted the condenser cooling water mode or the "second

siphon" from the CCW system design basis document, Specification

OSS-0254.00-00-0003, Rev 2, March 31, 1992. The licensee's

safety evaluation justifying the deletion, considered the

condenser cooling mode of decay heat removal as only required for

the total loss of power (onsite and offsite) event discussed at

original licensing. In the more recent SBO submittal approved by

the NRC (SER dated January 28, 1992), the decay heat removal

pathway described was via lifting main steam relief valves, and

not the condenser cooling mode. Therefore, the licensee

considered the SBO submittal as superseding the original

requirements.

Deletion of the condenser cooling mode was not justified because:

Technical Specifications 3.4.5 required the ECCW system.

The Technical Specification bases stated "Normally, decay

heat is removed by steam relief through the turbine bypass

system to the condenser. Condenser cooling water flow is

provided by a siphon effect from Lake Keowee through the

condenser for final heat rejection to the Keowee Hydro Plant

tailrace."

It also stated that, "Decay heat can also be

removed from the steam generators by steam relief through

the main steam safety relief valves." Therefore, both the

ECCW condenser cooling mode and the SBO submittal method

were credited for decay heat removal.

Section 9.2.2 of the current FSAR, "Cooling Water Systems,"

stated that the CCW system, "...serves as the ultimate heat

sink for decay heat removal during cooldown of the plant.

Following a design basis event involving loss of the CCW

pumps, the Emergency Condenser Circulating Water

System.. .provides flow through the condenser for decay heat

removal."

It further stated, "The CCW system has an

emergency discharge line to the Keowee hydro tailrace...

Under a loss-of-power situation, the emergency discharge

line will automatically open and the CCW system will

continue to operate as an unassisted siphon system supplying

sufficient water to the condenser for decay heat removal and

emergency cooling requirements." Additionally, it stated,

"...the "second siphon" provides flow through the condenser

to remove decay heat."

And finally it stated, "In a loss of

off-site power situation, the ECCW System is required to

function until a CCW pump can be manually restarted by the

control room operator."

The licensee's SBO submittal did not request elimination of

the ECCW condenser cooling mode from the licensing basis.

The NRC's SBO SER did not state relief was granted from

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17

previous condenser cooling mode licensing requirements, nor

did it state that the condenser cooling mode was only

required for a total loss of power event.

On page 9, item 6, of a May 23, 1993, Notice of Violation,

the NRC stated, "The ECCW system is required to provide both

a suction source to the Low Pressure Service Water (LPSW)

pumps and cooling water through the main condenser for decay

heat removal if the Condenser Circulating Water (CCW) pumps

are unavailable."

In a February 11, 1987, letter concerning an enforcement

conference for failure of an ECCW system test, the NRC's

position was summarized on Page 3 of Enclosure 1 as, "The

NRC discussed the event in detail with DPC and expressed

concern that the load shed test had not been appropriately

conducted in the past to insure that the required gravity

flow (which relies upon a siphon) for the ECCW System was

available and effective upon demand."

On this page, the

siphon referred to was defined as the "second siphon" in a

statement that, "The ECCW System relies upon a siphon effect

to lift water from Lake Keowee and then exit by gravity flow

to Lake Hartwell at a lower elevation."

The licensee stated that present practices (operation,

maintenance, testing, etc.) were not changed as a result of

deleting the condenser cooling mode from the design basis

document. However, the team considered that at a minimum, future

modifications could be impacted. Also, the minor modification's

safety evaluation became the basis for a licensee request to

delete ECCW from the Technical Specifications. The Technical

Specification change request was under review by NRR. Resolution

of the team's concerns associated with the licensing bases of the

condenser cooling mode and the prudence of the licensee's actions

are contingent upon NRR's decision (either approval or denial) of

the Technical Specification change request and completion of

NRC's review of Unresolved Item 50-269, 270, 287/93-13-03, "ECCW

System Design and Testing."

b. The CCW Pumps

(1) The active components associated with CCW pumps were not

classified as safety-related. However, the licensee credited CCW

pump operation 1/2 hour after accident occurrence to provide the

suction supply to the LPSW system. Therefore, the pumps were

improperly classified. Independently, the licensee recognized

the error and was classifying the pumps as safety related in the

most current draft revision to the Quality Standards Manual.

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18

Unresolved item 50-269, 270, 287/93-13-03, "ECCW System Design

and Testing," already identified concerns regarding the licensing

basis of the CCW pumps.

(2) The only documentation discussing CCW NPSH requirements was a

letter from the pump vendor which stated that the pump "...will

operate satisfactorily at a low water condition of elevation 770

feet."

This letter did not address the temperature of the water

on which this judgement was made. The design temperature for the

CCW pumps at the time of this letter is given in Table 9-12 of

the original FSAR as 750F. Since then, the design maximum lake

temperature was raised to 850F by Calculation OSC-2568, Revision

0, July 24, 1987. Also, the letter did not discuss operation

below the 770 feet elevation, the top of the intake canal's

underwater weir, which would be the initial conditions for the

loss of Keowee Dam event. Subsequently, the intake canal level

would decrease due to leakage and evaporation. Finally, the

intake canal temperature would steadily increase due to decay

heat and other heat input from the three units.

Prior to and during the inspection the licensee was attempting to

acquir, the necessary information from the pump manufacturer.

Acquisition of the information is Inspector Follow-up Item 5-269,

270, 287/93-25-09, "CCW Pump NPSH Information." The lack of CCW

pump performance evaluation during the loss of Keowee Dam event

is another facet of the inadequate Keowee Dam failure analysis

discussed in paragraph d. below.

(3) The power and control cables for all of the CCW pumps and the

pump discharge valves as well as all of the piping for the HPSW

supply to the pump seals and coolers were located in a common

trench at the CCW structure. This trench was covered with heavy

steel deck plates which were not bolted in place. In response to

a seismic event the plates in the horizontal portions of the

trench would not dislodge due to stiffeners welded to the plates.

However, there were sections of the trench running at

approximately 450 from horizontal, and the plates covering these

sections could be dislodged by a seismic event potentially

damaging the cables below. The licensee was able to demonstrate

that only the cables in the upper cable tray (powering the Unit 3

CCW pumps), and the cables in the bottom of the trench (powering

and controlling the CCW pump discharge valves) could be damaged.

Due to armored sheathing on the cables, damage could not spread

to adjacent cables from the resultant electrical faults.

Although CCW pump performance could be degraded, the total CCW

function of supplying water to the LPSW system and the condensers

would not be lost. The licensee initiated a work request to bolt

the covers in place.

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19

c. Keowee Loss of Dam Event

Part of the licensing bases for Oconee involved the ability to

withstand a loss of Lake Keowee as an ultimate heat sink. Section

10.4 of the original FSAR, "Condenser Circulating Water System"

stated, "In the unlikely event that the water level in Lake Keowee

should fall below 770 feet, an underwater weir in the intake canal

would act as a dam capable of retaining a large amount of water [67

million gallons] to serve as an emergency cooling pond. By operator

action, the condenser circulating water system normal discharge paths

would be closed and an emergency discharge conduit, provided for this

contingency, would be opened, permitting cooling by recirculation of

the cooling pond water. The capacity of this cooling pond is adequate

to provide core decay heat cooling indefinitely as long as electric

power is available to run the condenser cooling pumps in the intake

structure."

Therefore, for the dam break event, the impounded intake

canal would become the plant's ultimate heat sink.

Numerous weaknesses in the licensee's ability to respond to the Keowee

Dam failure were identified as discussed below.

(1) The licensee did not have analyses demonstrating the "...capacity

of this cooling pond is adequate to provide core decay heat

cooling indefinitely..."

Such analyses should have addressed

the heatup rate, the water inventory losses due to leakage,

evaporation, etc., and the effects of the increased temperature

and the decreased water inventory on the CCW system and the

various systems being served. Therefore, the licensee failed to

demonstrate the ability of the intake canal to perform as the

ultimate heat sink as described in the FSAR.

10 CFR 50, Appendix B, Criterion III, "Design Control," requires

in part that measures shall be established to assure that design

bases are correctly translated into design documents and

procedures. This is considered an example of violation 50-269,

270, 287/93-25-03E, "Failure to Perform Adequate Calculations and

Evaluations to Support Facility Design."

(2) Case B of Abnormal Procedure AP/1/A/1700/13, "Loss of Condenser

Circulating Water Intake Canal/Dam Failure," described the

actions to be taken in the event of a failure of the Keowee Dam

without loss of the CCW intake canal.

In Step 5.5.1, the

operator was directed to align the LPSW system to recirculate the

water back to the CCW crossover header between the units from

which it also takes suction in order to conserve circulating

water inventory.

In this closed loop condition, the temperature of the system

would rise very rapidly to the point where its ability to perform

its decay heat removal safety function would significantly

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20

degrade. The licensee had no analyses supporting operation in

this recirculation condition. Without such an analysis LPSW

system operation was inconsistent with system design

requirements.

10 CFR 50, Appendix B, Criterion III, "Design Control," requires

in part that measures shall be established to assure that design

bases are correctly translated into design documents and

procedures. This is considered an example of Violation 50-269,

270, 287/93-25-03F, "Failure to Perform Adequate Calculations and

Evaluations to Support Facility Design."

(3) Procedure AP/1/A/1700/13, Case B, "Dam Failure Without Loss of

Intake Canal", required the operator to actuate ECCW by pressing

the "CCW DAM FAILURE" pushbutton. This action tripped the CCW

pumps and opened the emergency discharge valve to the Keowee

tailrace, CCW-8, to establish the ECCW flow. Upon restoration of

power to the CCW pumps the operator was directed to start a CCW

pump, verify that CCW-8 closed, and verify the emergency

discharge to the CCW intake canal structure valve, CCW-9, opened.

However, as a consequence of the Keowee Dam failure valve CCW-8

would be submerged. Per Calculation FERC Project Number 2503

dated December 18, 1992, "Final Summary of Analysis to Determine

the Extent of Inundation Due to Catastrophic Dam Failure for

Keowee Hydro Project," for the dam failure event, the water level

at the valve would reach a maximum of 776 feet for the "sunny

day" failure and 785 feet for the "postulated maximum flood"

failure. Valve CCW-8 was located within the flooded area in a

concrete and steel enclosure. According to this calculation, the

valve would be submerged by as much as 55 feet, and 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />

would elapse before the water would recede below the valve. Even

with the receding water, the water, mud and debris trapped within

the enclosure could impact valve operation.

The licensee's analysis had not considered the consequences of

the dam failure affecting valve CCW-8. Subsequent licensee

review concluded that all operator actions associated with the

valve's cycling would be accomplished prior to the flood water

reaching the valve. However, the procedure and previous operator

training did not indicate that these actions were time dependent.

Also, the calculation establishing the time available for

operator action was not very precise. Therefore, the ability to

perform the necessary actions without such procedural

direction/training was questionable.

(4) Procedure AP/1/A/1700/13, "Loss of Condenser Circulating Water

Intake Canal/Dam Failure," had other weaknesses including:

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Pressing the "CCW DAM FAILURE" pushbutton without

considering CCW pump power availability in Case B. This

action tripped the CCW pumps and opened the emergency

discharge to the Keowee tailrace valve, CCW-8, to establish

the ECCW flow. However, tripping the CCW pumps with power

available was not necessarily the most appropriate action at

that time.

Not providing a caution to ensure a CCW pump was ready for

immediate restart prior to closing the CCW discharge valves.

Closure of the discharge valves would break the ECCW siphon.

Therefore, the CCW pumps must be immediately ready for

starting to maintain a viable decay heat removal path

through the condenser.

The licensee stated that procedure AP/1/A/1700/13 would be

reviewed to ensure procedural content was appropriate. Review

and revision of this procedure is considered part of Inspector

Follow-up Item, 50-269,270, 287/93-25-06B, "Actions to Improve

Operator Responses to Abnormal Events."

6. High Pressure Service Water System

The HPSW system was the site's fire protection system and constantly

supplied cooling and sealing water to the CCW pumps. The system was

capable of supplying cooling water to specific components normally cooled

by the LPSW system, such as the HPI pump motor coolers and the TDEFW pump

coolers. The system could also provide backup cooling to the Unit 1, 2,

and 3 LPSW systems, though at reduced capacity, through interconnections

at the discharge of the LPSW pumps.

The system was composed of three pumps, an elevated water storage tank

(EWST), and interconnecting piping to fire protection deluge valves

throughout the site and to the CCW pumps. The three HPSW pumps, two with

6000 gpm capacity each and one jockey pump, took suction from the 42 inch

CCW discharge header. The jockey pump was normally in service maintaining

HPSW system pressure. The other two pumps were in standby to

automatically makeup lost water inventory in the 100,000 gallon capacity

elevated storage tank.

HPSW must remain operational for the CCW system to accomplish its safety

related function of supplying water from the intake canal to the suction

of the LPSW pumps. The CCW system relied upon HPSW as a necessary support

system in both the siphon mode and CCW pump operating mode. The interface

between the CCW pumps and the CCW piping must be leaktight to prevent air

inleakage which would break the siphon. Seal water from HPSW performed

this function. Also, in order for the CCW pumps to operate, cooling water

must be supplied to pump motor bearing coolers. Cooling water from HPSW

performed this function. This sealing and cooling water was supplied by

the HPSW system normally through operation of the HPSW jockey pump, and

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22

during accident conditions involving a loss of power, from the elevated

water storage tank. The HPSW pumps also performed an accident mitigation

support function since EWST replenishment would be necessary to maintain

long term cooling and sealing flow to the CCW pumps.

The original NRC Safety Evaluation Report discussed the HPSW as a backup

to the LPSW system and "...concluded that the LPSW and HPSW systems will

provide all needed normal and emergency services and are acceptable."

Neither the SER nor the original FSAR discussed the HPSW support function

for the CCW system. In the more recent licensee SBO submittal and the

subsequent NRC SER, HPSW gravity flow cooling of CCW from the EWST for up

to four hours was assumed. Without continual gravity flow, air inleakage

would form voids requiring extensive fill and venting actions prior to CCW

pump restart. Therefore, to allow immediate pump restart after four

hours, the assumed duration of the SBO, HPSW gravity flow had to be

maintained.

Inspection findings associated with HPSW were:

a. The HPSW system was not classified, constructed, tested or maintained

commensurate with its importance to safety. This determination was

based upon:

(1) The HPSW system was not designated or constructed to the seismic

standards of the FSAR, but to conventional commercial fire

protection structural standards of the late 1960s.

Failure in

virtually any portion of the system in a loss-of-power event

would cause loss of CCW sealing and cooling water due to

diversion of flow out the faulted piping section depleting the

EWST water source. Consequently, through the loss of the siphon

or the CCW pumps, the LPSW and CCW decay heat removal

capabilities to all three units would be lost.

(2) The safety function of critical HPSW valves were not tested

following maintenance.

During a LOOP/LOCA, SBO or any LOOP, the HPSW pump check valves,

HPSW-2, 5, and 8, must not leak or the EWST inventory would drain

into the CCW suction header. Such leakage would directly impact

the duration of EWST cooling and sealing flow to the CCW pumps.

Maintenance records indicated that the only post maintenance

testing on these check valves was an external leakage observation

and did not include a reverse flow test. Normal system operation

would only indicate gross leakage of the main HPSW pumps' valves

and would not indicate any leakage of the jockey pump valve since

it operated continuously.

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23

Maintenance records for the last 13 years contained 5 work

requests associated with the check valves. Three involved the

HPSW jockey pump valve, HPSW-8. The first of these three was

written in 1982 to repair a seat leak on HPSW-8. Although the

original work request was lost, a replacement work request was

closed out on November 10, 1986, with a note to the effect that

the valve was checked out by Operations, and no problems were

found. However, on the next day, the second work request was

written to investigate and repair HPSW-8 because of indications

it was not seating. Under this work request, the disk was found

installed backwards and the disk nut and washer found to be

broken off. Since there were no replacement parts available, the

valve was reassembled and placed back into service on November

18, 1986, without a disk "...to enable [sic] the sys. to be

used."

Under the third work request, a replacement valve was

installed on January 23, 1987. Therefore, EWST cooling/sealing

capability to the CCW pumps was questionable for an extended

period of time. It also appeared that during the last two months

of this period, the inoperable status of this valve was

recognized by plant personnel without any compensatory measures

taken.

The other two work requests in the maintenance records were to

disassemble, inspect, and refurbish valves HPSW-5 and HPSW-2

respectively in 1990. A responsible Maintenance Supervisor was

asked if this work were being done today, would current

procedural requirements have specified post-maintenance back

leakage testing for these valves. He responded that it would not

have.

(3) Although the system performed a safety-related function, it was

not classified as safety-related in the licensee's safety

classification document, the Quality Standards Manual.

One of the ramifications of the lack of safety-related

designation was not including HPSW within the IST program.

Therefore, the stringent, periodic reverse flow testing of the

HPSW check valves was not required. Also, the HPSW system was

not included in much of the SWS GL actions since the GL was only

applicable to safety-related SWSs.

(4) CCW pump sealing flow indication was not properly maintained.

Consequently, operators may not be alerted to a low flow

condition jeopardizing siphon operation when required. Also, one

of the indications of inadequate motor bearing cooling flow was

not properly maintained.

Each of the 12 CCW pumps was instrumented with 2 rotameters. A

larger rotameter with a scribe mark was installed for sealing

flow and a smaller one without a scribe mark for cooling flow.

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24

These rotameters were input devices to low flow annunciators in

the control room. Also, operators took local rotameter readings

as part of their normal rounds.

Examples of improperly maintaining the rotameters were:

(a) The instrument procedure, IP/0/B/0261/004, used to calibrate

the low seal and cooling flow alarms, directed setting the

alarms nonconservatively with respect to the applicable

vendor information. The procedure directed setting the low

seal water alarm setpoint at 2.5 gpm + 0.5 gpm decreasing,

but the CCW pump vendor manual required a seal water flow of

3 to 5 gpm. The procedure directed setting the low bearing

cooling water alarm setpoint at 1.6 gpm + 0.2 gpm

decreasing, but the pump motor vendor drawing required a

bearing cooling water flow of 2.5 gpm.

Additionally, inconsistent with the rotameter's vendor

document, OM 267-0179, the procedure directed reading the

float from the bottom instead of from the scribe line on the

float or from the top if there was no scribe line.

(b) The material condition of some of the rotameters was poor.

Pump 2C's bearing cooler flow meter tube was installed

backwards with the scale in a difficult place to read.

Pumps 2A and 2D flow tubes, float, and guide rod for the

seal water flow meters were heavily coated with organic

contamination (slime).

This would tend to reduce the

accuracy of the instruments.

(c) The operator rounds sheet for taking local rotameter

readings contained no guidance on how to read the reference

marks. The Shift Manager was asked how the operators read

these gauges. He responded consistent with vendor guidance

on the larger rotameters with a scribe mark. However, he

stated that "It was the consensus of opinions of the

unlicensed operators that the float should be read to the

center of the cylindrical portion" for the smaller non

scribe mark types. As discussed earlier this was not the

correct reference point.

The seismic and safety classification concerns of the HPSW system were

encompassed in an outstanding unresolved item documented in NRC

inspection report 50-269, 270, 287/93-13. This unresolved item

concerned the licensing bases of the CCW pumps, the ECCW subsystem,

and their support systems. Resolution of this unresolved issue is

contingent upon further NRC review.

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25

b. Through various means (DBD effort, attempts to resolve outstanding

SITA issues on ECCW, and SBO submittal preparation) the licensee's

engineering organization recognized the safety significance of the

HPSW system. This was evident by the licensee's decision to evaluate

HPSW for seismic acceptability, adding the HPSW valves necessary for

CCW pump cooling and sealing to the most current draft revision of the

safety classification document and establishing a periodic disassembly

and inspection of the HPSW pump discharge check every fourth refueling

outage.

However, based upon interviews with operations and maintenance

personnel, this heightened safety emphasis on the HPSW system had yet

to be fully conveyed to the rest of the organization. Also, two of

the engineering actions associated with HPSW were not adequate or of

sufficient scope. The two actions are discussed below.

(1) In the licensee's most current draft revision to the Quality

Standards Manual, the safety classification document, some HPSW

components were included, but not the HPSW pumps or their

discharge check valves.

(2) The licensee recognized the lack of seismic qualification while

attempting to resolve ECCW siphon support system concerns during

design study ONDS 327 and PIP 92-084. The licensee concluded

that the HPSW system was structurally adequate because it was

"inherently rugged."

Inherently rugged was defined by the

licensee to mean that the system, in general, conformed to the

criteria in EPRI Report NP-5617, "Recommended Piping Seismic

Adequacy Criteria Based on Performance During and After

Earthquake," January 1988, which had yet to be endorsed or

accepted by the NRC. The licensee's evaluation criteria from the

EPRI report were:

A system walkdown has verified qualitatively that piping and

equipment in the system are adequately supported.

A system walkdown has verified that no large pipes are

restrained by small pipes.

A qualitative evaluation of the system has concluded that

corrosion does not threaten its structural integrity.

However, the licensee's evaluation failed to consider the

actuation of any of the fire deluge functions of the system due

to a seismic event, which would have the same effect as a pipe

break with regard to loss of water. Therefore, full

identification of the adverse condition and assurance of adequate

corrective action was not accomplished.

10 CFR 50, Appendix B,

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Criterion XVI, "Corrective Actions," requires conditions adverse

to quality be promptly identified and corrected. This is

considered an example of violation 50-269, 270, 287/93-25-04B,

"Inadequate Evaluation of Conditions Adverse to Quality by

Engineering."

Also, The licensee's evaluation involved these weaknesses:

The determination of adequate support was of a qualitative

nature. The team observed some of the HPSW piping at the

CCW intake structure to be supported by simple threaded rod

hangers at relatively long intervals, and the hangers were

attached to the concrete by simple expansion bolts.

The conclusion by the licensee that corrosion did not

threaten the structural integrity of the system was inferred

from observations made in the similar LPSW system, and can

be challenged by direct evidence of corrosion deterioration

in the HPSW system. Although through wall leakage had not

been observed, excessive flow restriction in the small bore

HPSW piping to the CCW pumps caused the piping material to

be upgraded to stainless steel in Exempt Change OE 4625.

The licensee's safety evaluation for this change stated,

"Recently failures have occurred in the small diameter

piping, showing that the corrosion has reached the condition

of causing us to question the integrity of the pipe."

Also,

though it did not render the system inoperable, corrosion

had been identified in the LPSW system.

Only the portion of the system from the HPSW water source to

the CCW pumps was included in the walkdown.

The seismic and safety classification concerns of the HPSW system

were encompassed in an outstanding unresolved item documented in

NRC inspection report, 50-269, 270, 287/93-13. This unresolved

item centered around the licensing bases of the CCW pumps, the

ECCW subsystem, and their support systems. The lack of seismic

qualification for the HPSW system was specifically discussed in

the report.

The concept of "inherently rugged" as an acceptable

substitute for seismic qualification is another aspect of this

unresolved issue. Resolution of this unresolved issue is

contingent upon further NRC review.

c. There were numerous weaknesses in the management controls that assured

the HPSW system was capable of performing as indicated in the

licensee's SBO submittal.

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The SBO submittal discussed gravity flow cooling of the CCW pumps from

the EWST for up to four hours so the CCW pumps could be restarted

immediately upon restoration of offsite power. Without continual

gravity flow, air inleakage would form voids requiring extensive fill

and venting actions prior to starting the CCW pumps.

The management control weakness are discussed below.

(1) The ability to perform cooling via the EWST to the CCW pumps and

other necessary equipment for four hours was tested annually

using test procedure PT/0/A/250/38, "Elevated Water Storage Tank

Drain Test."

Per Section 8.2 of the procedure and the design

specification for HPSW, OSS-0254.00-00-1002, the normal level of

the EWST was 90,000 gallons or greater. Per Enclosure 13.3 of

the procedure, Step 5.0, the capacity of the tank in minutes was

calculated by dividing the EWST level at the beginning of the

test by the adjusted HPSW outleakage flow rate. The result must

be greater than 240 minutes (4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />) to be acceptable. However,

using the level at the beginning of the test for the calculation

rather than the minimum full level of 90,000 gallons, only

verified that the tank had sufficient capacity at that particular

time, not for any other time when the level may be lower but

still in the normal range above the "full" 90,000 gallons level.

For the last six tests (March 21, 1987-August 7, 1993) the tank

level varied between 87,500 gallons and 99,100 gallons.

Therefore, the procedure failed to establish the appropriate

initial test conditions. The licensee's submittal of January 26,

1990, states that adequate test procedures will be established to

ensure system performance during a SBO.

This is Deviation 50

269, 270, 287/93-25-10, "Inadequate HPSW SBO Test."

(2) The EWST drain test procedure had additional problems including:

0

It allowed test re-performance if the original test failed

due to HPSW discharge check valve leakage. Prior to test

re-performance the procedure directed the applicable pump be

isolated (closing its discharge valve) thus isolating the

leaking check valve.

Following completion of this second

test, the isolated pump could be returned to service with an

annotation on the operator turnover sheets to isolate the

applicable pump on a loss of power event to prevent

excessive losses of the EWST.

This method of assuring EWST cooling capability by isolating

the pump was not directed by emergency procedures, did not

provide for verification of the completed action and could

be forgotten or overlooked due to the numerous other tasks

associated with a LOOP or SBO event. Also, assuming the

operator action was performed, there was no provision in the

test's acceptance criteria to account for the EWST inventory

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28

lost through the leaking check valve prior to isolating the

pump. Therefore, the procedure allowed an equipment

deficiency that directly affected the test's acceptance

criteria to be excluded without proper compensation.

It directed the user to inform the operating manager for

leakage rates greater than 500 gpm, rather than the maximum

acceptable leakage rate of 375 gpm. Also, there was no

direction as to what action the operating manager was to

take upon being notified of the excessive flowrate. In an

interview with an operating manager, he did not know what

the appropriate response would be.

(3) For over seven months, the four hour gravity feed capability

lacked validation. On February 27, 1993, PT/O/A/250/3 was

performed and the system failed to meet the 240 minute acceptance

criteria by 45 minutes. Subsequently, the licensee recognized

that the procedure did not account for several water loss points

from the system which automatically isolate for a loss-of-power

event. The procedure was revised to account for these inventory

losses on April 27, 1993. However, even when accounting for

these losses, the test on February 27, 1993, would not have met

the acceptance criteria. On August 7, 1993, the test was

successfully re-performed. The team could not ascertain what

(system maintenance, improper recording of data, change in

equipment performance, etc.) caused the difference between the

adjusted test results of February 27th and August 7th test

results. The licensee was unable to provide any insights.

(4) Five of the CCW seal water rotameters and all of the bearing

cooling water flows (3A's was solid against the upper stop at 8+

gpm) were greater than the values used to calculate the four hour

availability of the EWST. Also, the operator rounds

sheets

contained no upper limit for these flows.

7. Standby Shutdown Facility

The SSF was a separate onsite building housing the necessary equipment to

maintain all three units in a safe shutdown condition following turbine

building flood, fire, sabotage, certain classes of tornados or station

blackout. The SWS portion of the SSF was composed of a high head, low

capacity pump and interconnecting piping to all steam generator EFW

discharge lines, solenoid operated flow control valves in the discharge

lines to the steam generators, a pump and piping to cool a tandem diesel

with a common generator, two pumps with a condenser unit to cool the HVAC

within the SSF and a moveable submersible pump. The SSF ASW, HVAC and EDG

pumps took suction from the Unit 2's CCW pumps discharge header. The HVAC

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and EDG pumps discharged to the CCW header. There was an option to divert

the EDG pump discharge water to the yard drainage system when high

temperature constraints warranted. The submersible pump allowed

replenishment of the CCW header from the intake canal.

a. Jocassee Dam Failure

In the licensee's IPE submittal for an event outside the facility's

licensing bases, the SSF was discussed as the system to mitigate the

consequences of a Jocassee Dam failure. This dam was located upstream

of the Oconee site and formed the uppermost boundary of Lake Keowee.

The IPE flood evaluation concluded that the Oconee site would be under

4.71 feet of water. With the exception of the SSF, this would render

all decay heat removal cooling systems inoperable. To assure the SSF

would not be affected by the flood, a 5-foot (4.71-foot plus

0.29-foot) high waterproof flood wall was constructed around the

ground level entrances to the SSF. The review of the SSF to withstand

this postulated flood was as follows:

(1) Contrary to the IPE submittal, the SSF could not withstand the

postulated flood. Therefore, core damage of all reactor units

would occur as a consequence of such a postulated flood.

In response to questions from the team regarding initial lake

height assumptions, the licensee stated that a recently completed

reanalysis of the Jocassee Dam failure for another regulatory

agency resulted in a flood height at least 10 feet above the SSF

wall.

The change in flood height was due to modeling a bridge

abutment downstream of the Keowee tailrace in the most recent

flood analysis. The abutment acted as a flow constriction

causing the flood waters to backup over the Oconee site. From a

PRA perspective the probability of core melt from the Jocassee

Dam failure as calculated by the team increased ten fold to

1.58E-05.

Licensee correction of the this error and subsequent corrective

actions as a result of the error are considered a part of

Inspector Follow-up Item 50-269, 270, 287/93-25-11A, "Jocassee

Dam Failure IPE Inaccuracies."

(2) Another aspect of the IPE submittal was in error. IPE Submittal

report, Section 3, Subsection 13, indicated there was an 8-foot

waterproof flood wall around the SSF ground level entrances. The

wall was 5-foot in height.

Licensee correction of the this error and subsequent corrective

actions as a result of the error is considered a part of

Inspector Follow-up Item 50-269, 270, 287/93-25-11B, "Jocassee

Dam Failure IPE Inaccuracies."

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(3) A watertight gate was installed in the flood wall to allow access

to and from the SSF. The gate was observed on more than one

occasion with the watertight dogs not properly secured.

b. SSF Calculations

(1) Following plant modifications performed in previous years, some

of the applicable calculations were not updated. Examples

included:

OSC-2030, Standby Shutdown Facility HVAC Load Calculations

The calculation conclusion section stated:

"The SSF Air Conditioning System can maintain design

conditions in the safety related areas (Control Room and

Battery Rooms) with the following actions:

(A) Start second condenser circulating water pump to

provide 41 GPM condenser water flow with both pumps

operating.

(B) Shed security computer load by the time control room

temperature reaches 85 F or temperature of condenser

water reaches approximately 93 F."

However, an electrical interlock had been installed

preventing simultaneous operation of the two condenser

circulating water pumps. The condenser circulating water

pumps were of different sizes, and their simultaneous

operation would cause flow instability and eventual pump

runout.

This interlock could not be bypassed. Also, the

SSF HVAC system had been modified excluding portions of the

security complex and portions of the HVAC had been rerouted.

Prior to the conclusion of the inspection the licensee re

performed the HVAC calculation with acceptable results. The

design document had not reflected the as-built condition of

the facility at the time of the inspection.

OSC-3233, SSF Service Water System Hydraulic Model

The last revision of the model was January 23, 1989. Since

then, the HVAC pump motors had been changed from 1750 rpm to

3600 rpm motors, pressure breakdown orifices had been

installed, the 3 way valves located upstream of the SSF HVAC

condensers had been replaced, and the SSF ASW impellers had

been changed twice. Other calculations were performed which

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partially encompassed the changes to the hydraulic model

but, did not reconcile those results with the total

hydraulic model.

Therefore, this design document did not

reflect the as-built condition of the facility.

The administrative controls for updating calculations, EDM-101,

Engineering Calculations/Analysis, Section 2.4.4 only required

these calculations be updated in a timely manner, rather than

establishing a definitive length of time.

10 CFR 50, Appendix B,

Criterion V, "Instructions, Procedures, and Drawings," require

appropriate acceptance criteria for determining that quality

related activities have been satisfactorily accomplished. This

is an example of Violation 50-269, 270, 287/93-25-12A, "SWS

Procedure/ Drawing Content or Procedure Implementation

Inadequacies."

(2) Calculation OSC-4171, "SSF ASW Pump Minimum Flow Line Design

Inputs Calculation," contained invalidated or nonconservative

assumptions as follows:

Each unit or steam generator pair had only one flow

instrument associated with it. Calculation OSC-3303, "SSF

ASW Flow and SSF ASW Pump Suction Pressure, Instrument

Accuracy Calculation: CCW FT0225," determined the

methodology for calculating the instrument loop error for

the flow instruments. The result was +/- 54 gpm for an

individual flow instrument. The three flow instruments

errors were averaged through the square root sum of the

squares method resulting in an error of +/- 31 gpm. The

instrument error used in calculation OSC-4171 was +/- 31

gpm.

However, if just one of the flow instruments were at or near

it's negative maximum error that particular unit's minimum

required flow would be inadequate. According to accepted

industry methodology, the square root sum of the squares

methodology is used to combine dependent and independent

variables to calculate loop uncertainties. In this instance

the methodology was misapplied, in that it was used to

reduce an individual error contribution and not calculated

loop uncertainties. The use of this nonconservative

assumption resulted in a flow to a pair of steam generators

that was 23 gpm below the minimum analyzed flow. During the

inspection period the licensee indicated that a calculation

was being prepared that would lower the minimum required

flows such that the 23 gpm difference would not invalidate

the conclusion of OSC-4171. However, the calculation was

not ready for NRC review. 10 CFR 50, Criterion III, "Design

Control," requires the design basis and applicable

regulatory requirements be translated into appropriate

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documents. This is considered an example of Violation 50

269, 270, 287/93-25-03G, "Failure to Perform Adequate

Calculations and Evaluations to Support Facility Design."

Calculation OSC-4171 assumed the flows were equally balanced

between all six generators. That assumption had never been

validated.

Calculation OSC-4171 and numerous other calculations assumed

certain flow distributions among the three SWS operating

pumps (SSF ASW, HVAC, and EDG cooling water pump). Also,

the discharge flow of the operating HVAC pump was assumed to

equally split between the two parallel SSF HVAC condenser

coolers. These two assumptions had not been validated.

c. SSF Testing

(1) Post-construction Testing

Post-construction SSF testing in the mid-1980s did not adequately

confirm critical functional requirements of the SSF design and

was not performed in accordance with committed quality standards.

Examples included:

(a) The flushing procedure provided by the licensee for the

discharge lines was a gravity fill and drain from HPSW prior

to the piping being connected at the SSF ASW pump discharge

or in the penetration rooms. There was no acceptability

criteria for the flush in the procedure. This fill and

drain did not provide assurance that the lines were not

blocked or partially restricted.

(b) The calculations supporting SSF design assumed certain

flowrates and flow distributions to the steam generators.

No documentation existed validating that flow could be

achieved to any of the steam generators. The licensee

verbally confirmed that there was no flow testing performed

which involved the discharge lines beyond the test line

connection. Therefore, flow control valve capabilities were

not verified, and assumptions associated with equalizing

flow to units and steam generator pairs were not verified.

(c) The calculations supporting SSF design assumed certain flow

distributions among the three SWS operating pumps (SSF ASW,

HVAC and EDG cooling water pump). The three pumps were not

tested simultaneously to confirm the assumed flow

distributions and that the equipment would perform as

predicted.

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The preoperational testing portion of ANSI N45.2.8-1975,

Section 5.2, dealing with assurance of operation in

accordance with SSF design and proper flow alignments was

also applicable to this aspect of the facility's design.

10 CFR 50, Appendix B, Criterion XI, "Test Control," requires a

preoperational testing program demonstrating facility

acceptability to the design requirements. Also, the licensee was

committed to ANSI N45.2.8-1975 and ANSI N45.2.1-1973 through Duke

Power Company Topical Report 1-A, Table 17.0-1. ANSI N45.2.8

1975Property "ANSI code" (as page type) with input value "ANSI N45.2.8</br></br>1975" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process. and ANSI N45.2.1-1973 requires in part that flushing

procedures with velocities and acceptance criteria based on

filter, turbidimetric or chemical analyses. The preoperational

testing portion of ANSI N45.2.8-1975, Section 5.2, states in part

"This testing involves the operation of all items in a system ...

to assure that operation is in accordance with the design

criteria and functional requirements. The testing shall include,

but not be limited to, ... service requirements for initial

operation such as flow alignments ... " Therefore, critical

aspects of the SSF's design were not demonstrated prior to

placing the facility into service. This is an example of

Violation 50-269, 270, 287/93-25-088, "Inadequate SSF and ECCW

Testing."

(2) Periodic Testing

(a) The periodic testing program for the SSF was accomplished

through component specific testing. There were specific

tests for the SSF ASW pump, HVAC pump, etc., which were

performed at different test intervals. The periodic SSF ASW

pump test discharged through a test line connection and not

through the full extent of the steam generator discharge

lines. Therefore, the deficiencies of the post-construction

testing previously discussed in paragraph c.1 above were not

rectified by the periodic test program.

b. Beyond the post-construction testing deficiencies discussed

in paragraph c.1, the sum of the component specific periodic

testing did not constitute an integrated test. Certain

aspects of system design could only be provided by the

licensee through the completion of actions during emergency

response drills. An example of this was the unwinding and

connecting of the submersible pump's electrical cable to its

emergency bus and operating the pump. These actions were

not part of any periodic test program and had only been

accomplished once during an emergency response drill.

c. Emergency Procedure AP/O/A/1700/25, Standby Shutdown

Facility Emergency Operating Procedure, Enclosure 6.1, Step

2.5 and 2.12 instructed the operator to start the SSF ASW

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Pump with no preparatory action beyond aligning a flow path

to the designated unit. The periodic pump operability test,

PT/O/A/0400/05, directed an additional action of pump

venting in Step 12.2 just prior to starting the pump in Step

12.4. This action preconditioned the pump, possibly masking

air entrapment within the pump which would affect pump

performance.

10 CFR 50, Appendix B, Criterion XI, "Test

Control," requires test procedures direct the establishment

of suitable environmental conditions when performing the

test. This is considered an example of Violation 50-269,

270, 287/93-25-08C, "Inadequate SSF and ECCW Testing."

d. Other Observations

(1) There were few material condition deficiencies observed.

Preventive and corrective maintenance was effective. Repetitive

corrective maintenance actions were not evident. Most work

requests were completed in one to three months.

(2) Operator training met normal industry standards and emphasized

strict adherence to procedures. The information supplied by

training matched the information in the procedure.

8. Auxiliary Service Water System

ASW was originally designed for a non-design bases event, the loss of the

intake canal/structure. However, following NUREG 0737 review of the

facility for tornado vulnerabilities, the system was discussed in the July

28, 1989, NRC Safety Evaluation Report to mitigate the consequences of the

most severe classes of tornadoes.

For these severe tornados the ASW

system in conjunction with the HPI system were required to maintain the

units in a safe shutdown condition by providing adequate decay heat

removal via the steam generators and RCS makeup.

ASW was a shared system common to all three units. It consisted of a

suction connection at the Unit 2 CCW pump discharge piping, a low head,

high capacity pump, piping with manual valves connected to the EWF

discharge piping of all three units for cooling all the steam generators,

and piping with manual valves connected to the LPSW piping for cooling the

HPI pump motor coolers. The ASW pump was operated from the tornado

protected, safety related AuxService Water Switchgear.

The only other actions necessary in the severe tornado event was operation

of the HPI pump. Since normal HPI pump power was not tornado protected,

one HPI pump motor per unit could be manually connected to the AuxService

Water Switchgear through spare power cables staged for this purpose.

Inspection findings associated with the ASW system were:

a. Emergency Procedure EP/1,2,3/A/1800/01, Section 502, Step 10.1

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required approximately 200 gpm be provided to each steam generator by

the ASW pump. The step further stated that if one steam generator was

isolated, flow should be increased to approximately 400 gpm to the un

isolated steam generator. The ASW discharge lines or the

interconnection with the EFW system to the steam generators did not

contain any flow instruments. Therefore, there was no way to verify

the directed actions had been accomplished.

10 CFR 50, Appendix B,

Criterion V, "Instructions, Procedures and Drawings," requires

adequate written procedures be provided for activities affecting

quality. This is an example of Violation 50-269, 270, 287/93-25-12B,

"SWS Procedure/Drawing Content or Procedure Implementation

Inadequacies."

b. To support the licensee submittal that ultimately led to the tornado

SER, Calculation OSC-2262, Tornado Protection Analysis, was generated.

The calculation indicated that ASW system operation must be

accomplished in about 40 minutes to prevent core uncovery.

(1) Job performance measures existed for the alignment of ASW to the

steam generators, alignment of ASW to the HPI pump motor coolers,

and establishment of electrical power to a HPI pump motor.

Documentation indicated that the tasks could be accomplished in

approximately 30 minutes after the operators recognized the need

for ASW. No integrated drill/test verifying that all the tasks

could be accomplished within the requisite time had been

performed.

(2) There was no abnormal procedure specifically for a tornado event.

Entrance into the emergency operating procedures for inadequate

secondary side heat transfer would eventually direct use of the

ASW system. These procedures attempted to establish normal

feedwater, emergency feedwater, and SSF service water prior to

initiation of ASW. However, there was only 10 minutes available

for the operator to direct initiation of ASW in lieu of these

other systems (10 minutes to decide to use ASW + 30 minutes to

initiate ASW from training documentation = 40 minutes before core

uncovery).

The procedure provided the system options, but system

selection was based on operator judgement depending upon the

extent of the tornado damage. No test or drill had been devised

confirming the operator's ability to make this judgement within

the 10 minutes available.

(3) Other procedures associated with flow through the EFW header to

the steam generators included a caution to limit flow to less

than 1000 gpm to reduce tube vibration. Procedures associated

with ASW operation did not contain such cautions and the

hydraulic model indicated that flow to the Unit 3 steam

generators would exceed 1000 gpm in certain conditions. The

licensee indicated that flows of this magnitude would be for a

short period and the tube integrity concerns due to vibration

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were only a factor in extended operation. However, the licensee

decided to review this item and determine if procedural guidance

should be included.

Licensee initiatives to improve operator guidance for response to a

severe tornado are considered a part of Inspector Follow-up Item, 50

269,270, 287/93-25-06C, "Actions to Improve Operator Responses to

Abnormal Events."

c. Certain equipment associated with the ASW system were not included

within a periodic testing program. However, licensee actions

associated with the DBD effort identified the situation and

appropriate corrective actions were being taken. Examples included:

Cooling water flow to the HPI pump motors had never been

established using the ASW system. However, a test procedure was

being developed to establish and verify flow to the HPI motor

coolers.

Certain check valves within the LPSW system which must close to

establish HPI flow were not tested in the closed direction per

the IST program. This lack of reverse flow check valve testing

had been previously identified by the licensee. Corrective

actions were in progress to revise the IST program and develop

testing procedures for the valves. This is Violation 50-269, 270

287/93-25-13, "Omissions of LPSW Check Valves from IST Program."

However, based upon the corrective actions in progress, the

licensee's self identification of the matter, no similar

violations associated with omissions in the IST program, the lack

of willfulness, and the nonescalated enforcement nature of the

violation, this is considered a non-cited violation authorized

under 10 CFR 2, Appendix C, Section VII.B.2.

The discharge check valves to the steam generators were being

incorporated into a test/inspection program for the first time.

d. Some of the calculations associated with the ASW system lacked rigor.

Examples included:

(1) Calculation OSC-4989, Auxiliary Service Water Flow Model, did not

model cooling water flow to the HPI pump motors. The licensee

performed preliminary calculations indicating flow would be

sufficient. Also, complete bench marking of the ASW hydraulic

flow model had not been performed.

(2) In the formal ASW pump NPSH analysis and in a subsequent informal

analysis the licensee used incorrect assumptions. These were:

Report Details

37

(a) Calculation OSC-5125, ASW NPSH Analysis, assumed siphon flow

from the intake canal to the ASW pump suction would be in

operation following the tornado. Consequently, an

administrative minimum level, 780', associated with Lake

Keowee was selected as the minimum suction height for the

NPSH calculation. However, the ECCW siphon lacked tornado

protection, and would not be operational. Therefore, the

minimum suction height was contingent upon the inventory

losses in the CCW piping as a result of ASW pump operation.

(b) Once the incorrect assumption was identified to the

licensee, the licensee re-evaluated the situation and

determined the minimum NPSH for the ASW pump was -2.22 psig

and NPSH considerations did not restrict pump operation. A

required NPSH of -2.22 psig meant that the pump could draw

water from 5.12 feet below the pump's impeller eye and still

have adequate NPSH. However, the licensee failed to

consider the actual configuration of the CCW piping going to

the suction of the ASW pump. Therefore, when the water in

the CCW piping dropped to a height of 770.46 feet,

inadequate NPSH would occur.

Subsequently, the licensee performed preliminary calculations of

the water volume between 791 feet, the assumed initial suction

height of the calculation, and 770.46 feet. Results indicated

that a substantial amount of water inventory still existed

allowing ASW operation for an extended period. Therefore, the

assumed replenishment of the ASW supply source before reaching

770.46 feet appeared reasonable. Issuance of a revised

calculation is considered an Inspector Follow-up Item 50-269,

270,287/93-25-14, "Review of Revised ASW Pump NPSH Calculation."

(3) Abnormal Procedure AP/1,2,3/A/1700/11, Loss of Power, Enclosure

6.3, Aux Service Water to HPI Pump Motor Coolers, required the

recirculation test line valve, CCW-247, be opened approximately 2

turns prior to starting the ASW pump. This flow path through the

test line was also the minimum flow pathway to prevent

deadheading the pump. No data or calculations existed showing

that enough flow could be achieved with CCW-247 throttled to

protect the pump. Subsequently, the licensee performed

preliminary calculations indicating a flow between 400 and 450

gpm could be achieved with valve CCW-227 in the throttled

position. The 400 gpm flow appeared acceptable for minimum flow

protection. However, the licensee decided to completely open

CCW-247, fully assuring minimum flow protection, prior to

starting the ASW pump.

Report Details

38

9. Keowee Hydroelectric Station

Lake Keowee was the motive and cooling source for the two hydroelectric

generators which functioned as Oconee's onsite emergency power. Water

flowed from a common penstock, through the turbines and into the tailrace.

Cooling flow came from a single pipe located in the penstock. Once the

line entered the building housing the hydroelectric units it split into

two lines, one for each unit. Cooling flow for the turbine bearing oil

cooler, the stuffing box, eight thrust bearing heat exchangers and six

generator air coolers came from the unit specific main line.

Inspections findings associated with Keowee were:

a. Corrective Actions

Previous NRC inspections identified that numerous aspects of the

quality assurance program had been omitted from Keowee. In response

to NRC observations the licensee established an integrated corrective

action plan entitled the "Emergency Power Management Plan."

Prior to

the management plan, the licensee had initiated design study ONDS 258

to correct design document deficiencies at Keowee. ONDS 258 was not

part of the committed Emergency Power Management Plan.

(1) Under the design study the licensee revised the Keowee Turbine

Generator Cooling Water System drawings, KFD-100A-1.1 and KFD

100A-2.1. However, errors were still present on the drawings

including an inconsistent piping class break in the supply line

to the thrust bearing coolers, the connection of the supply line

to the air compressor coolers on Unit 1 was indicated in the 12

inch portion of the main line instead of the 8" portion, a valve

downstream of valve 2WL-3 for Unit 2 was not indicated even

though one was present, and the piping downstream of WL 76 in

both units was indicated as carbon steel instead of copper.

Subsequently, the licensee initiated a condition adverse to

quality report to correct drawing errors. 10 CFR 50, Appendix B,

Criterion V, "Procedures, Drawings, and Instructions," requires

in part that drawings reflect the as-built condition of the

facility. This is considered an example of Violation 50-269,

270, 287/93-25-12C, "SWS Procedure/Drawing Content or Procedure

Implementation Inadequacies."

(2) Numerous errors existed in the I&C portion of drawings KFD-100A

1.1 and KFD-100A-2.1 and other related I&C drawings. The I&C

drawing update portion of the design study was in progress and

the licensee had already identified these same discrepancies for

resolution. It was noted that the I&C drawing update portion of

design study had not been met. As stated previously, the design

study was not part of the committed Emergency Power Management

Plan. Also, there was no definitive mechanism to assure the I&C

drawings (part of the design study) were correct prior to

Report Details

39

transferring instrument calibration responsibilities from the

Keowee staff to the Oconee staff (part of the Emergency Power

Management Plan).

Prior to the end of the inspection period the

two organizations involved discussed the situation and the

licensee indicated that the appropriate integration would occur.

(3) Although the valve positions observed at Keowee were -consistent

with design requirements, no operating procedures existed for the

mechanical systems reviewed. Therefore, no specific procedural

controls existed for the throttled, manual valves in the

generator air and thrust bearing discharge lines. The Keowee

staff was aware of this deficiency and planned to generate

procedures in the future. Also, the safety significance of this

situation was reduced since these valves were locked throttled

and rarely manipulated. However, the creation of these

procedures was not identified as a corrective action under the

management plan or the design study.

b. Turbine Bearing Oil Cooler Maintenance

During the inspection period, the licensee removed the Unit 2 safety

related turbine bearing oil cooler from service to perform the

triennial cleaning and inspection. While reinstalling the cooler, a

coupling was broken and required replacement prior to completing the

installation. Subsequently, a condition adverse to quality report was

initiated.

(1) As part of the response to the adverse condition report,

engineering personnel discussed Unit operability without the

turbine bearing oil cooler installed. Engineering personnel

verbally determined that the cooler was only needed during

extended high ambient temperature conditions (the summer) and

unit operability was not effected. However, Nuclear Generation

Department Directive 2.8.1, "Problem Investigation Process," step

3.4 directed that adverse conditions requiring engineering

assistance be processed as an upper tier adverse quality report

which receive a written operability evaluation. Subsequently,

the cooler was reinstalled in the unit for emergency operation

and PIP 93-0994 initiated for not performing the written

operability evaluation.

10 CFR 50, Appendix B, Criterion V,

"Drawings, Procedures and Instructions,"

requires in part that

established procedures be followed. This is considered an

example of Violation 50-269, 270, 287/93-25-12D, "SWS Procedure/

Drawing Content or Procedure Implementation Inadequacies."

(2) The work request for oil cooler maintenance specified

housekeeping zone 4 for the cleanliness requirements. However,

Oconee Nuclear Site Directive 1.4.1, "Cleanliness in Safety

Related Areas," Section 3.1, stated the highest level zone

designation allowed for safety related equipment was 3. The

Report Details

40

difference between level 3 and 4 was zone 4 lacked personnel and

tool accountability. A review of numerous completed safety

related work requests on other equipment revealed that zone 4 was

routinely designated. Contrary to the 10 CFR 50, Appendix B,

Criterion V, "Instructions, Procedures and Drawings,"

requirements for procedure adherence, the licensee did not

designate the correct housekeeping zones on safety related work

requests. This is an example of Violation 50-269, 270, 287/93-25

12E, "SWS Procedure/Drawing Content or Procedure Implementation

Inadequacies."

c. Other Observations

(1) The scope of the calibration program was weak. Annunciator

actuation was not verified in any of the calibration procedures

reviewed and the licensee stated that this was generally the case

with all calibration procedures at Keowee. Generator and thrust

bearing cooling flow setpoints and the associated timers were not

checked. The transmitter for the packing box's local pressure

indicator was not being calibrated. The licensee indicated that

these procedures would be reviewed for improvement. However, the

description of the instruments being calibrated and how they

affected system operation in individual calibration procedures

was complete, accurate and well written.

(2) Historically, the mechanical systems at Keowee performed well.

Little corrective maintenance was needed. Preventative

maintenance was appropriate and consistent with operating

experience and vendor manual recommendations where applicable.

The hydroelectric station was operated almost daily. The daily

operation functioned as a performance test in many respects and

placed much of the mechanical systems under no worse conditions

than would be experienced when operating as an emergency power

source. However, no equipment performance trending, especially

of the safety related heat exchangers, was being performed.

(3) One common mode failure vulnerability was identified. Within the

common stretch of piping for cooling both units' mechanical

support systems was a manual gate valve.

Prior to the end of

this inspection the licensee locked the valve open.

(4) Minimal housekeeping and material condition discrepancies were

observed. Personnel were knowledgeable of their safety-related

duties.

10. Miscellaneous Matters

Findings not tied to a particular system were:

Report Details

41

a. The DBD concept and the associated testing acceptance criteria was a

good initiative by the licensee. Generally, the DBDs provided the

best description of the system, the system's function, the licensee's

understanding of the licensing bases and the design requirements.

There were, however, some implementation weaknesses resulting in

errors and discrepancies in the DBDs. Also, the licensee partially

attributed the lack of reconciliation and failure to update the SSF

calculations to the lack of a completed DBD for the SSF.

b. There were FSAR omissions which could have clarified and more

completely explained the actual design parameters for select

components. An example was the flow to the RBCUs which the FSAR

discussed as 1400 gpm whereas, certain testing configurations only

exhibited 800 gpm flow and the system was considered as performing its

design function.

c. Offsite review committee minutes contained the proper content,

indicated that a proper quorum was present and met within the required

frequency. Resumes indicated that personnel qualification

requirements were met. Committee performance was consistent with

regulatory requirements.

d. Design calculation OSC-3528, Establish an Administrative Minimum Lake

Level for Keowee, contained unsubstantiated and nonconservative

assumptions, and a variety of other calculational irregularities. The

licensee indicated that the calculation was a theoretical "look see"

calculation and the title was misleading. There were no other

calculations associated with minimum Lake Keowee water volume.

Further licensee initiatives to perform an actual analytical

calculation to establish a minimum Lake Keowee level to assure

adequate water volume is maintained is Inspector Follow-up Item

50-269, 270, 287/93-25-15, "Administrative Controls for Lake Keowee."

11. Follow-up on Previously Identified Items

(Open) Unresolved Item 50-279, 270, 287/93-13-03, "ECCW System Design and

Testing":

Sections 5.a.3, 5.a.7, 5.b.1, 6.a., and 6.b.2 discussed

different aspects of this matter. However, further NRC review is

necessary to ensure any regulatory action taken is consistent with the

original licensing requirements.

12. Exit Interview

The team conducted an exit meeting on December 14, 1993, at the Oconee

Nuclear Power SLation to discuss the major areas reviewed during the

inspection, the strengths and weaknesses observed, and the inspection

results.

Licensee representatives and NRC personnel attending this exit

meeting are documented in Appendix A of this report. The team also

discussed the likely informational content of the inspection report. The

licensee did not identify any documents or processes as proprietary.

Report Details

42

There were dissenting comments at the exit meeting associated with

recommended regulatory action concerning the inadequate NPSH conditions in

the LPSW pumps and the possible regulatory action involving the lack of

dual turbine building isolation in the LPSW system. The licensee

indicated a thorough review of the inspection findings would be necessary

to ascertain the appropriate responses or corrective actions to the issues

identified. Also, on February 3, 1994, NRC management discussed the

unresolved LPSW turbine building isolation issue with the licensee via

telephone.

ITEM NUMBER

STATUS

PARAGRAPH

DESCRIPTION

93-25-01

Open

3

DEV - Failure to Adequately

Perform SWS GL Actions

93-25-02

Open

4.a.1

UNR - Turbine Building

Isolation Single Failure

Vulnerabilities

93-25-03

Open

4.b.1,

VIO - Failure to Perform

4.e,

Adequate Calculations and

5.a.4,

Evaluations to Support

5.c.1,

Facility Design

5.c.2,

7.b.2

93-25-04

Open

4.c.3,

VIO - Inadequate

6.b.2

Evaluation of Conditions

Adverse to Quality by

Engineering

93-25-05

Open

4.d

IFI - Additional Validation of

RBCU Evaluation Inputs

93-25-06

Open

4.f.2,

IFI - Actions to Improve

5.c.3,

Operator Responses to

8.b.3

Abnormal Events

93-25-07

Closed

5.a.1

NCV - Inadequate

Classification of Siphon

Support Equipment for LPSW

Supply

93-25-08

Closed

5.a.5,

VIO - Inadequate SSF and

7.c.1.c,

ECCW Testing

7.c.2.c

93-25-09

Open

5.b.2

IFI -

CCW Pump NPSH

Information

Report Details

43

93-25-10

Open

6.c.1

DEV - Inadequate HPSW SBO Test

93-25-11

Open

7.a.1,

IFI - Jocassee Dam

7.a.2

Failure IPE Inaccuracies

93-25-12

Open

7.b.1,

VIO - SWS

8.a

Procedure/Drawing Content or

Procedure Implementation

Inadequacies

93-25-13

Closed

8.c

NCV - Omissions of LPSW Check

Valves from IST Program

93-25-14

Open

8.d.2

IFI - Review of Revised ASW

Pump NPSH Calculation

93-25-15

Open

10.d

IFI - Administrative Controls

for Lake Keowee

93-13-03

Open

11

UNR - ECCW System Design and

Testing

APPENDIX A

Duke Nuclear Power Plant

Persons Contacted

L. Azzarello, Mechanical/Nuclear Engineering

S. Baldwin, Systems Engineer -

Raw Water

H. Barron, Station Manager - Oconee Nuclear Station

R. Colainanni, Nuclear Licensing - General Office

D. Coyle, Systems Engineering Manager

J. Davis, Safety Assessment

B. Dolan, Mechanical/Nuclear Engineering Manager

P. Farish, Nuclear Engineer -

PRA

K. Grayson, Mechanical/Nuclear Engineering

J. Hampton, Vice President - Oconee Nuclear Station

H. Harling, Mechanical/Nuclear Engineering

R. Harris, Senior Engineer -

Systems Engineering

J. Hemminger, Mechanical/Nuclear Engineering

M. Hipps, Mechanical Maintenance

D. Hubbard, Component Engineer

D. Kelley, Civil Engineering

R. Ledford, Instrumentation and Controls

T. Ledford, Electrical Engineering

E. LeGette, Operations

G. McAninch, Systems Engineer

S. Nader, Mechanical/Nuclear Engineering

M. Patrick, Regulatory Compliance Manager

D. Patterson, Regulator Compliance -

Oconee Nuclear Station

B. Peele, Engineering

M. Tuckman, Senior Vice President -

Nuclear Generation

J. Weir, Component Engineer

U.S. Nuclear Regulatory Commission

L. Mellen, Reactor Inspector

D. Prevatte, Powerdyne Corporation

C. Rapp, Reactor Inspector

W. Rogers, Team Leader

L. King, Reactor Inspector

A. Gibson, DRS Division Director

M. Lessor, DRP Section Chief

L. Weins, NRR Licensing Project Manager

P. Harmon, Senior Resident Inspector

K. Portner, Resident Inspector

L. Keller, Resident Inspector

  • Indicates those present at the exit meeting on December 14, 1993

APPENDIX B

Generic Letter 89-13 Action Items

I.

Biofouling Control and Surveillance Techniques

Action I of GL 89-13 requested licensees to implement and maintain an

ongoing program of surveillance and control techniques to significantly

reduce the incidence of flow blockage problems as a result of

biofouling. The actions requested included intake structure

inspections, periodic SWS flushing/flow testing and chemical treatment

of the SWS.

SWS Intake Structure Biofouling Inspections - The licensee had developed

a program to monitor, sample, and analyze the intake structure for

Asiatic clams. This program was conducted once per refueling cycle or

annually. The program had identified the presence of clams but at a low

population density. There was no increasing trend in the number of

clams. Also, some minor corrective maintenance in the LPSW, SSF and

HPSW systems had been due to clam presence. The team considered the

program adequate.

Periodic SWS Flushing/Flow Testing - The licensee had implemented a flow

testing and piping inspection program to identify reduced and blocked

flow to equipment. Hydraulic models had been developed for the ASW, SSF

and LPSW systems. No periodic flushing program was established.

LPSW - The licensee's efforts had been very effective in identifying

inadequate flow to numerous pieces of LPSW equipment through small bore

piping. The hydraulic model had been fully benchmarked. However,

instrument impulse lines had been excluded from the program. The

corrective maintenance history indicated repeated instrument failures

due to flow blockage. Subsequent actions under the SWS Steering

Committee recognized the situation and prompted revision to the

instrument calibration procedures to include flushing. Revision of the

procedures was scheduled for completion in March, 1994. Also, without a

flush program the LPSW crosstie line between Units 1/2 and 3 received no

evaluation. As a result of other regulatory correspondence this section

of stagnant piping was to be inspected and flushed at the next refueling

outage.

Other Systems - The benchmarking of the SSF hydraulic model was

incomplete with respect to the SSF diesel service water pump portion of

the flow model and the SSF ASW pump discharge piping to the steam

generators. The hydraulic model of the ASW system excluded the piping

to the HPI pump motor coolers. Also, the flow downstream of the

discharge valves to the steam generators had not been benchmarked. No

program had been developed for the Keowee SWSs.

SWS Chemical Treatment - The licensee's biofouling monitoring program

did not indicate a level of clam infestation that would warrant chemical

treatment.

Appendix B

2

II. Monitoring Safety Related Heat Exchanger Performance

Action II of GL 89-13 requested licensees to implement a test program to

periodically verify the heat transfer capability of all safety related

heat exchangers cooled by the SWS. The test program was to consist of

an initial test program and a periodic retest program.

In response to this item, the licensee established a performance

monitoring program for LPSW heat exchangers. The program was a

combination of inspections, performance tests and computer modeling.

The program specifics and the team assessment were:

Low Pressure Injection Coolers - These coolers were tested during each

refueling outage when the coolers were placed in service for decay heat

removal.

This test was conducted at a heat load less than would be

experienced during accident conditions. A fouling factor was developed

based on the test results and compared to historical data to identify

any adverse trend that would indicate increasing fouling.

The team considered the LPI cooler performance monitoring as adequate.

Reactor Building Cooling Units - To determine operability of the RBCUs,

the licensee used a computer code to predict the heat removal under

accident conditions based on heat removal data taken during normal

operations.

The team had two concerns with this process. The first concern was the

ability of the computer code to predict RBCU heat removal under accident

conditions. This computer code was divided into two separate

calculations. First, a fouling factor was calculated based on data

taken during normal operations. The fouling factor was then used to

predict the heat removal during accident conditions. Because the

airflow distribution was non-uniform, the licensee used another computer

code that predicted the airflow distribution based on the data taken

during normal operating conditions. This computer code was obtained

from a vendor and the licensee relied on the vendor's benchmarking of

the computer code. A non-regulatory required airflow test performed in

1987, indicated the airflow was substantially less than assumed in the

computer code; however, the licensee stated this test was invalid due to

significant air side fouling. The ability of this computer code to

accurately predict the air flow distribution has a direct effect on RBCU

operability.

The second concern was the accuracy of LPSW flow measurement. The

determination of RBCU heat removal capability relied on the accuracy of

the LPSW flow measuring device which was an installed orifice. The

inspectors reviewed documentation and photographs that showed the LPSW

Appendix B

3

piping had fouled at various points. A reduction in the diameter of the

piping in the area of the orifice would result in higher indicated LPSW

flow. The licensee had performed a special test to determine the

accuracy of the LPSW flow instrumentation by subtracting the indicated

flows from other LPSW supplied components from the total LPSW flow;

however, this resulted in unrealistically high LPSW flow to the RBCUs.

The licensee also performed testing of the LPSW pumps using ultrasonic

flow measurements which indicated substantially lower flows than the

installed instrumentation. The licensee stated this was a special test

for gathering data and did not constitute a valid performance test.

The team concluded that without field validation of the RBCU airflow

distribution and stronger-assurance of flow element accuracy, the RBCU

computer results were questionable.

Small LPSW Heat Exchangers - Periodic flow verifications were performed.

The team had no concerns.

The Main Condensers - The main condenser were cleaned and inspected each

refueling outage. The team had no concerns.

SSF Diesel Engine Jacket Water Heat Exchangers - The ISI requirements

for the SSF diesel lube oil and jacket water coolers was on a 10 year

cycle verses the 5 year criteria in the GL. No other monitoring program

was in place. The team considered the performance monitoring of these

heat exchangers inadequate.

SSF HVAC Condensers - A semiannual preventive maintenance activity for

the SSF air handling unit required cleaning of the condenser tubes if

the head saturation temperature was more than 10OF higher than the

outlet temperature. The licensee stated the condenser tubes had not

been cleaned based upon the above conditions. The team had no concerns.

Keowee - No formal performance monitoring of the SWS heat exchangers had

been established. In the licensee's informal SWS Program Manual the

Keowee heat exchangers were discussed indicating that normal operation

of Keowee by operators would identify any problems. The team considered

the present monitoring methods as inadequate.

First, the

instrumentation that would be relied upon to inform the operators of a

problem was not being fully maintained as discussed in Section 9.c.1.

Second, there was no documented trending or operator rounds program in

place for the SWS heat exchangers.

In summary the heat exchanger performance monitoring program had been

inadequately implemented, mainly due to a lack of scope.

Appendix B

4

III.

Routine Inspection and Maintenance

Action III of GL 89-13 requested that licensees implement a routine

inspection and maintenance program for open-cycle SWS piping and

components. This program was to ensure that corrosion, erosion,

protective coating failure, silting, and biofouling would not degrade

the performance of the safety related systems supplied by the SWS.

In response to this action item, the licensee had established periodic

inspections, cleaning as needed, and piping replacements.

Piping - Design Study ONDS-252 evaluated SWS piping configurations for

the sections with the highest potential for corrosion. The criteria for

determining the most probable area of corrosion was piping material,

piping diameter, duration of flow through the pipe and velocity of flow.

Corrective action in the form of stainless steel piping replacements was

accomplished in a number of the potential corrosion areas. Also, an

aggressive program of pipe section inspections were in place. With the

help of the SWS Steering Group a Service Water Piping Corrosion

Management Program Manual dated October 29, 1993, had been developed to

assure appropriate management control and attention were maintained for

this effort. This piping inspection program did not include the Keowee

SWSs. No other program encompassed Keowee.

The team considered the piping inspection and replacement program

excellent except in terms of scope. This caused the licensee's actions

to be inadequate due to the omission of the Keowee SWS piping from the

program. For the systems where licensee actions were applied the

maintenance program was adequate except in select equipment associated

with the HPSW system and the CCW pumps. These pieces of equipment

suffered from inadequate safety classification that reduced the rigor of

assurance that the materials used in repair activities were proper and

the work was performed properly. This also included the rigor used in

post maintenance testing.

Pumps and Valves - Following the 1987 SITA a preventive maintenance

schedule for the LPSW pumps was established. However, pump rebuild and

refurbishment could not be accomplished within the TS LCO time allowed

which caused maintenance constraints on the shared Unit 1/2 LPSW system.

Pump performance deficiencies had centered around high temperatures in

the stator of the motors. The CCW pumps were experiencing long term

vibration/fatigue with adequate corrective actions being taken to

address the issue. Valves were being adequately maintained.

Heat Exchangers -

Periodic inspections and cleaning frequencies had

been established for a number of heat exchangers.

Appendix B

5

IV. Design Function Verification and Single Failure Analysis

Action IV of GL 89-13 requested to licensees confirm that the SWS would

perform its intended function in accordance with the licensing basis for

the plant. This confirmation was to include a review ensuring requisite

safety functions were accomplished even with the failure of a single

active component.

In response to this action item, the licensee utilized the 1987 self

assessment of the LPSW system and the ECCW support (first siphon) to the

LPSW system. Also, design calculations were performed to verify that

safety functions were accomplished with a single failure occurring.

The team considered the LPSW design review of the 1987 self-assessment

as thorough and comprehensive. However, some of the corrective actions

did not adequately address the issues identified such as isolation of

the LPSW turbine building header. Resolution to problems identified

while implementing corrective actions to the self-assessment were

occasionally inadequate as with the inadequate NPSH for the LPSW pumps

and the postulated waterhammer in the RBCU discharge piping. Also, a

number of corrective actions were untimely such as safety classification

of the CCW pumps and, seismic suitability of the vacuum priming and HPSW

systems which support ECCW (first siphon) operation. The self

assessment did not include the ASW, SSF SWS, Keowee, HPSW, and the other

operating modes of the CCW system (second siphon and loss of Keowee

Dam).

In summary the licensee's corrective actions to this action item

were inadequate.

V.

Training

Action V of GL 89-13 requested licensees to confirm that maintenance

practices, operating and emergency procedures, and training involving

the SWS were adequate to ensure safety related equipment cooled by the

SWS would function as intended.

In response to this action item the licensee evaluated LPSW maintenance

practices, all LPSW operating (normal and abnormal) procedures, and LPSW

training, as part of the 1987 self-assessment. Beyond this specific .

review, the licensee considered the established personnel qualification

2 year procedure review, 10 CFR 50.59 safety evaluation, qualified

reviewer, operating experience and operator requalification programs as

adequate to address this action item.

The team identified LPSW weaknesses which were within the scope of this

aspect of the 1987 self-assessment. Examples of these weaknesses

included the lack of an abnormal procedure addressing inadequate LPSW

flow and, limited operator training on containment temperature concerns

during an accident. Also, beyond the specific self-assessment, the

established generic programs did not identify numerous weaknesses.

Examples of these weaknesses included the lack of operating procedures

Appendix B

6

for Keowee SWSs, weak operator direction in response to the Keowee Dam

failure, the inability to verify flow to the steam generators from the

ASW system and incomplete verification that ASW actions could be

accomplished within the 40 minute required timeframe. A review, similar

to that performed on the LPSW system, of Keowee would almost certainly

have identified the lack of key quality assurance elements in the

operation, maintenance and training associated with the Keowee

hydroelectric station years before operational events in 1992 brought

them to light. In summary the licensee's corrective actions to this

action item were inadequate.

APPENDIX C

Acronyms and Abbreviations

ANSI

American National Standards Institute

ASW

Auxiliary Service Water

BWST

Borated Water Storage Tank

CCW

Condenser Circulating Water

CC

Component Cooling Water

CGD

Commercial Grade Dedication

DBD

Design Basis Document

DEV

Deviation

DPC

Duke Power Company

ECCW

Emergency Circulating Cooling Water

EDG

Emergency Diesel Generator

EFW

Emergency Feedwater

EP

Emergency Procedure

EPRI

Electric Power Research Institute

ESF

Engineered Safety Feature

EWF

Emergency Feedwater

EWST

Elevated Water Storage Tank

FSAR

Final Safety Analysis Report

GL

Generic Letter

GPM

Gallons per Minute

HPI

High Pressure Injection

HPSW

High Pressure Service Water

HVAC

Heating, Ventilation, and Air Conditioning

IFI

Inspector Follow-up Item

IPE

Individual Plant Examination

ISI

Inservice Inspection

IST

Inservice Test

LCO

Limiting Condition for Operation

LER

Licensee Event Report

LOCA

Loss of Coolant Accident

LOOP

Loss of Offsite Power

LPI

Low Pressure Injection

LPSW

Low Pressure Service Water

MTOTC

Main Turbine Oil Temperature Control

NCV

Noncited Violation

NPSH

Net Positive Suction Head

PRA

Probabilistic Risk Assessment

PSIA

Pounds per Square Inch Absolute

PSIG

Pounds per Square Inch Gauge

RBCU

Reactor Building Cooling Unit

RCS

Reactor Coolant System

SBO

Station Blackout

SER

Safety Evaluation Report

SSF

Safe Shut Down Facility

SWS

Service Water System

SWSOPI

Service Water System Operational Performance Inspection

TDEFW

Turbine Driven Emergency Feedwater

TDH

Total Developed Head

TS

Technical Specification

UNR

Unresolved

VIO

Violation