ML101650723
| ML101650723 | |
| Person / Time | |
|---|---|
| Site: | Calvert Cliffs |
| Issue date: | 06/14/2010 |
| From: | David Lew Division Reactor Projects I |
| To: | George Gellrich Constellation Energy Nuclear Group |
| References | |
| EA-10-080 IR-10-006 | |
| Download: ML101650723 (45) | |
See also: IR 05000317/2010006
Text
UNITED STATES
NUCLEAR REGULATORY COMMISSION
REGION I
475 ALLENDALE ROAD
KING OF PRUSSIA, PA 19406*1415
June 14, 2010
George H. Gellrich, Vice President
Calvert Cliffs Nuclear Power Plant, LLC
Constellation Energy Nuclear Group, LLC
1650 Calvert Cliffs Parkway
Lusby, Maryland 20657-4702
SUBJECT:
CALVERT CLIFFS NUCLEAR POWER PLANT - NRC SPECIAL INSPECTION
REPORT 05000317/2010006 AND 05000318/2010006; PRELIMINARY WHITE
FINDING
Dear Mr. Gellrich:
On April 30, 2010. the U. S. Nuclear Regulatory Commission (NRC) completed a Special
Inspection of the February 18, 2010, dual unit trip at Calvert Cliffs Nuclear Power Plant
(CCNPP) Units 1 and 2. The enclosed report documents the inspection results, which were
discussed on April 30, 2010, with you and other members ofyour staff.
The special inspection was conducted in response to the dual unit trip with complications on
February 18, 2010. The complications included loss of a 500 kilovolt (kV) offsite power supply
to each unit, loss of power to a 4 kV safety bus on each unit, failure of the 2B emergency diesel
generator (EDG) to reenergize a 4 kV safety bus, loss of power to the Unit 24 kV non-safety
buses, loss of Unit 2 forced reactor coolant system (RCS) flow, and loss of the Unit 2 normal
heat sink. The NRC's initial evaluation of this event satisfied the criteria in NRC Inspection
Manual Chapter 0309, "Reactive Inspection Decision Basis for Reactors," for conducting a
special inspection. The Special Inspection Team (SIT) Charter (Attachment 2 of the enclosed
report) provides the basis and additional details concerning the scope of the inspection.
The special inspection team (the team) examined activities conducted under your license as
they relate to safety and compliance with Commission rules and regulations and with conditions
of your license. The team reviewed selected procedures and records, observed activities,
conducted in-plant equipment inspections, and interviewed personnel. In particular, the team
reviewed event evaluations (including technical analyses), causal investigations, relevant
performance history, and extent-of-condition to assess the Significance and potential
consequences of issues related to the February 18 event.
The team concluded that, overall, station personnel maintained plant safety in response to the
reactor trips. Nonetheless, the team identified several issues related to equipment performance
and human performance which complicated the event. The enclosed chronology (Attachment 3
of the enclosed report) provides additional details on the sequence of events and event
complications.
G. Gellrich
2
This report documents one self-revealing finding that, using the reactor safety Significance
Determination Process (SDP). has preliminarily been determined to be White, a finding with low
to moderatE~ safety significance. The finding is associated with the failure to perform appropriate
maintenanc:e activities to ensure 2B EDG reliability. Specifically, safety related time delay
relays in th~:: EDG low lube oil pressure trip circuit were used beyond the manufacturer
recommended service life. without an associated test or monitoring program to demonstrate_
their continued reliability. Consequently, when called upon to reenergize the 24 4 kV safety
bus, the time delay relay failed and the 2B EDG prematurely tripped in response to a low lube
oil pressure signal. The 24 4 kV safety bus was reenergized from an alternate feed source
approximately 30 minutes into the event. The significance determination of the event was
performed assuming that similar time-delay relays on other systems have not failed due to this
performance deficiency. Subsequent corrective actions included replacing and retesting the
associated time delay relays on all three EDGs susceptible to the low lube oil pressure trip.
There is no current immediate safety concern due to this finding. because all EDGs have
subsequently been demonstrated operable and long term corrective actions are being
implemente1d through the Calvert Cliffs corrective action program to address the extent-of
condition and extent-of-cause. The final resolution of this finding will be conveyed ina separate
correspondence addressing the final risk significance and disposition of any violations.
As discussed i~ the attached inspection report. the finding is also an apparent violation (A V} of
NRC requirements, involving Technical Specification 5.4.1, and is therefore being considered
for escalated enforcement action in accordance with the Enforcement Policy, which can be
found on NRC's Web site at http://www.nrc.gov/reading-rom/doc-cotlections/enforcementi.
In accordance with NRC Inspection Manual Chapter (lMC) 0609, we will complete our
evaluation using the best available information and issue our final determination of safety
significanc: within 90 days of the date of this letter. The significance determination process
encourages an open dialogue between the NRC staff and the licensee; however, the dialogue
should not impact the timeliness of the staffs final determination.
Before we make a final decision on this matter, we are providing you with an opportunity (1 ) to
attend a Regulatory Conference where you can present to the NRC your perspective on the
facts and assumptions the NRC used to arrive at the finding and assess its significance, or (2)
submit your position on the finding to the NRC in writing. If you request a Regulatory
Conference, it should be held within 30 days of your response to this letter and we encourage
you to submit supporting documentation at least one week prior to the conference in an effort to
make the conference more efficient and effective. If a Regulatory Conference is held. it will be
open for public observation. If you decide to submit only a written response. such submittal
should be s,ent to the NRC within 30 days of your receipt of this letter. If you deCline to request
a Regulatory Conference or submit a written response, you relinquish your right to appeal the
final SDP dE~termination,in that by not doing either, you fail to meet the appeal requirements
stated in the Prerequisite and Limitation sections of Attachment 2 of IMC 0609. We request that
if you decide to attend a Regulatory Conference or provide a written response, that you address
the apparent violation, and that you also address the length of time that the 28 EDG was
considered inoperable.
Please contact Glenn Dentel at (610) 337-5233 in writing within 10 days from the issue date of
this letter to notify the NRC of your intentions. If we have not heard from you within 10 days, we
wHl continue with our significance determination and enforcement decision. The final resolution
of this matter will be conveyed in separate correspondence.
G. Gellrich
3
Because the NRC has not made a final determination in this matter, no Notice of Violation is
being issued for these inspection findings at this time. In addition, please be advised that the
number and characterization of the apparent violation described in the enclosed inspection
report may change as a result of further NRC review.
In addition, the report documents two NRC-identified findings and two self-revealing findings,
each of very low safety significance (Green). Three of these findings were determined to
involve violations of NRC requirements. However, because of the very low safety significance
and because they are entered into your corrective action program, the NRC is treating these
findings as non-cited violations (NCVs) consistent with Section VI.A.1 of the NRC Enforcement
Policy. If you contest any NCV, you should provide a response within 30 days of the date of this
inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, AnN.:
Document Control Desk, Washington DC 20555-0001; with copies to the Regional
Administrator, Region I; the Director, Office of Enforcement, United States Nuclear Regulatory
Commission, Washington, DC 20555-0001; and the NRC Senior Resident Inspector at Calvert
Cliffs Nuclear Power Plant. In addition, if you disagree with the characterization of any finding in
this report, you should provide a response within 30 days of the date of this inspection report,
with the basis for your disagreement. to the Regional Administrator, Region I, and the NRC
Senior Resident Inspector at Calvert Cliffs Nuclear Power Plant. The information you provide
will be considered in accordance with Inspection Manual Chapter 0305.
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its
enclosure, and your response (if any) will be available electronically for public inspection in the
NRC Public Document Room or from the Publicly Available Records (PARS) component of
NRC's document system .(ADAMS). ADAMS is accessible from the NRC Website at
http://www.nrc.gov/reading-rm/adams.html(the Public Electronic Reading Room).
Sincerely,
I:t.~Ml~
Division of Reactor Projects
Docket Nos.: 50-317. 50~318
License Nos.: CPR-53, DPR-69
Enclosure:
Inspection Report 05000317/2010006 and 05000318/2010006
w/Attachments: Supplemental Information (Attachment 1)
Special Inspection Team Charter (Attachment 2)
Detailed Sequence of Events (Attachment 3)
cc w/encl:
Distribution via ListServ
Enclosure:
Inspection Report 05000317/2010006 and 05000318/2010006
G. Gellrich
3
Because the NRC has not made a final determination in this matter, no Notice of Violation is
being issued for these inspection findings at this time. In addition, please be advised that the
number and characterization of the apparent violation described in the enclosed inspection
report may change as a result of. further NRC review.
In addition, the report documents two NRC-identified finding and two self-revealing findings,
each of very low safety significance (Green). Three of these findings were determined to
involve violations of NRC requirements. However, because of the very low safety significance
and because they are entered into your corrective action program, the NRC is treating these
findings as non-cited violations (NCVs) consistent with Section Vl.A.1 of the NRC Enforcement
Policy. If you contest any NCV, you should provide a response within 30 days of the date of this
inspection report, with the basis for your denial. to the Nuclear Regulatory Commission, ATTN.:
Document Control Desk, Washington DC 20555-0001; with copies to the Regional
Administrator, Region I; the Director, Office of Enforcement, United States Nuclear Regulatory
Commission, Washington, DC 20555-0001; and the NRC Senior Resident Inspector at Calvert
Cliffs Nuclear Power Plant. In addition, if you disagree with the characterization of any finding in
this report, you should provide a response within 30 days of the date of this inspection report,
with the basis for your disagreement. to the Regional Administrator, Region I. and the NRC
Senior Resident Inspector at Calvert Cliffs Nuclear Power Plant. The information you provide
will be considered in accordance with Inspection Manual Chapter 0305.
In accordance with 10 CFR 2.. 390 of the NRC's "Rules of Practice," a copy of this letter, its
enclosure, and your response (if any) will be available electronically for public inspection in the
NRC Public Document Room or from the Publicly Available Records (PARS) component of
NRC's document system (ADAMS). ADAMS is accessible from the NRC Website at
http://www.nrc.gov/reading-rm/adams.html{the Public Electronic Reading Room).
Sincerely,
IRAJ
David C. Lew. Director
Division of Reactor Projects
Docket Nos.:
50~317. 50-318
License Nos.: OPR-53, DPR~69
Enclosure:
Inspection Report 05000317/2010006 and 05000318/2010006
w/Attachments: Supplemental Information
Special Inspection Team Charter
Detailed Sequence of Events
cc w/encl:
Distribution via ListServ
Distribution w/encl (see attached page)
SUNSI Review Complete:
GTD
(Reviewer'S Initials
DOCUMENT NAME: G:\\DRP\\BRANCH1\\CalverLCllffs\\CC SIT Report 2010-06 Final.doc
After declarin this document "An OffiCial
enc Record*, it will be released to the Public.
OFFICE
R!/DRP
RI/DRS
RIIDRP
NAME
DKern/dk via
WCooklwc
06114110
06/14/10
RI/DRP
JClifford~c
NColeman/nc via email SWeeerakkody!sw via
!
emllil
06f14/10
06/14/10
06114/10
OFFICIAL RECORD COPY
G. Gellrich
Distribution:
S. Collins, RA
M. Dapas, DRA
L Trocine, RI OEDO
J. Lubinski, NRR
G. Dentel, DRP
N. Perry, DRP
J. Hawkins, DRP
D. Lew, DRP
J. Clifford, DRP
4
S. Kennedy, DRP, Senior Resident Inspector
M. Davis, DRP, Resident Inspector
C. Newgent, DRP, Resident M
Region I Docket Room (with concurrences)
ROPResources@nrc.gov
L Pinkham, DRP
D. Kern, DRP, Senior Resident Inspector
1
Docket No.:
license No.:
Report No.:
Licensee:
Facility:
Location:
Dates:
Team Leader:
Team:
Observers:
Approved By:
U. S. NUCLEAR REGULATORY COMMISSION
REGION I
50-317
50-318
05000317/2010006, 05000318/2010006
Constellation Generation Company
Calvert Cliffs Nuclear Power Plant (CC)
Lusby, Maryland
February 22, through April 30. 2010
D. Kem. Senior Resident Inspector, Division of Reactor Projects (DRP)
W. Cook, Senior Reactor Analyst, Division of Reactor Safety (DRS)
M. Patel, Reactor Inspector. DRS
P. Presby, Reactor Inspector, DRS
B. Smith, Resident Inspector, DRP
R. Montgomery, Reactor Engineer, Nuclear Safety Professional
Development Program, DRP (added subsequent to issuance of the
Inspection Charter)
S. Gray, Power Plant Research Program Manager, Department of Natural
Resources, State of Maryland
M. Griffen, Nuclear Emergency Preparedness Coordinator, Department of
the Environment, State of Maryland
Glenn T. Dentel, Chief
Projects Branch 1
Division of Reactor Projects
Enclosure
2
TABLE OF CONTENTS
SUMMARY OF FINDINGS .............................................................................................................3
REPORT DETAilS.........................................................................................................................7
1.
Background and Description of Events .,. ........................................................................7
2.
Equipment Performance .................................................................................................8
3.
Human Performance .....................................................................................................21
4.
Organizational Response ..............................................................................................25
5.
Risk Significance of the Event. ......................................................................................27
40A3
Follow~up of Events ......................................................................................................28
40A6 Meetings, Including Exit ................................................................................................28
SUPPLEMENTAL INFORMATION............................................................................................. 1-1
KEY POINTS OF CONTACT...................................................................................................... 1-1
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED .......................................................... 1-1
LIST OF D()CUMENTS REVIEWED .......................................................................................... 1-2
LIST OF ACRONYMS ................................................................................................................ 1-5
SPECIAL INSPECTION TEAM CHARTER ................................................................................ 2-1
DETAILED SEQUENCE OF EVENTS ........................................................................................ 3-1
Enclosure
3
SUMMARY OF FINDINGS
IR 05000317/2010006 and 05000318/2010006; 02/22/2010 - 04/30/2010; Constellation
Generation Company, Calvert Cliffs Nuclear Power Plant; Special Inspection for the February
18,2010. Dual Unit Trip; Inspection Procedure 93812, Specia/lnspection.
A six-pe~on NRC team. comprised of resident inspectors, regional inspectors, and a regional
senior reactor analyst conducted this Special Inspection. The team was accompanied by two
engineers from the State of Mary/and, Department of Natural Resources and Department of the
Environment. One apparent violation with potential for greater than Green safety significance
and four Green findings were identified. The significance of most findings is indicated by their
color (Green, White, Yellow, or Red) using Inspection Manual Chapter (IMC) 0609, 'Significance
Determination Process' (SOP); the crosscutting aspect was determined using IMC 0310,
'Components Within the Cross Cutting Areas;' and findings for which the SOP does not apply
may be Green or be assigned a severity level after NRC management review. The NRC's
program for overseeing the safe operation of commercial nuclear power reactors is described in
NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006.
NRC Identified and Self Revealing Findings
Cornerstone: Initiating Events
- ~: A self-revealing non-cited violation (NCV) of 10 CFR Part 50, Appendix B,
Criterion XVI "Corrective Actions," was identified, because auxiliary building roof leakage
into the Unit 1 and Unit 2 45 foot switchgear rooms was identified on several occasions
from 2002 to 2009, but was not thoroughly evaluated and corrective actions to this
condition adverse to quality were untimely and ineffective. This degraded condition led
to the failure of the auxiliary building to provide protection to several safety related
systems from external events, a ground on a reactor coolant pump (RCP) bus, and
ultimately a Unit 1 reactor trip. Immediate corrective actions included: repair of
degraded areas of the roof; walk downs of other buildings within the protected area that
could be susceptible to damage to electrical equipment due to water intrusion; issuance
of standing orders to include guidance regarding prioritizing work orders due to roof
leakage; and identifying further actions to take during periods of snow or rain to ensure
plant equipment is not affected. Constellation entered the issue into their corrective
action program (Condition Report (CR) 2010-001351). Long-term corrective actions
include implementation of improved plant processes for categorization, prioritization and
management of roofing issues.
The finding is more than minor because it is associated with the protection against
external factors attribute of the Initiating Events Cornerstone and affected the
cornerstone objective to limit the likelihood of those events that upset plant stability and
challenge critical safety functions during shutdown as well as power operations. The
team determined the finding had a very low safety significance because, although it
caused the reactor trip, it did not contribute to the likelihood that mitigation equipment or
functions will not be available. The cause of the finding is related to the crosscutting
area of Problem Identification and Resolution, Corrective Action Program aspect P.1 (c)
because Constellation did not thoroughly evaluate the problems related to the water
intrusion into the auxiliary building
Enclosure
4
such that the resolutions addressed the causes and extent-of-condition. This includes
properly classifying, prioritizing, and evaluating the condition adverse to quality. (Section
2.1)
- Green: The team identified a finding for failure to translate the design calculations of
phase overcurrent relays on 13 kV feeder breakers into the actual relay settings. The
overcurrent relays protect the unit service transformer against faults in the primary or
secondary side windings. The design specified limit of 1200 amps was determined
based on the breaker rating of the feeder breakers. Constellation determined the as
found relay setting for the feeder breakers was 1440 amps which exceeded the rating of
the feeder breakers. The team determined that due to the as-found relay setting, certain
phase overcurrent conditions could potentially cause the breakers to fail prior to the
phase overcurrent relay sensing the degraded condition. This condition could affect the
recovery of the safety buses from the electrical grid. Constellation entered this issue into
the corrective action program (condition report 2010-002123).
The finding is more than minor because it affected the Initiating Events Cornerstone
attribute of equipment performance for ensuring the availability and reliability of systems
to limit the likelihood of those events that upset plant stability and challenge critical
safety functions during shutdown as well as power operations. Also, this issue was
similar to Example 3j of IMC 0612, Appendix E, "Examples of Minor Issues," because
the condition resulted in reasonable doubt of the operability of the component, and
additional analysis was necessary to verify operability. This finding was determined to
be of very low safety significance because the design deficiency did not result in an
actual loss of function* based on Constellation's determination that the maximum load
current possible would not challenge the feeder breaker ratings. Enforcement action
does not apply because the performance deficiency did not involve a violation of a
regulatory requirement. The finding did not have a cross-cutting aspect because the
most significant contributor to the performance deficiency was not reflective of current
licensee performance. (Section 2.3)
Cornerstone: Mitigating Systems
Preliminary White: The NRC identified an apparent violation of Technical Specification 5.4.1 for the failure of Constellation to establish, implement, and maintain preventive
maintenance requirements associated with safety related relays. The team identified
that Constellation did not implement a performance monitoring program specified by the
licensee in Engineering Service Package (ES2001 00067) in lieu of a previously
established (in 1987) 1 O-year service life replacement PM requirement for the 28 EDG
T3A time delay relay. As a consequence, the 26 EDG failed to run following a demand
start signal on February 18, 2010. Following identification of the failed T3A relay, it was
replaced and the 28 EDG was satisfactorily tested and returned to service. In addition,
time delay relays used in the 1 Band 2A EDG protective circuits, that also exceeded the
vendor recommended 1 O-year service life, were replaced. Constellation entered this
issue, including the evaluation of extent-of-condition, into the corrective action program.
This finding is more than minor because it is associated with the equipment performance
attribute of the Mitigating Systems Cornerstone and adversely impacted the objective of
ensuring the availability, reliability, and capability of the safety related 2B EDG to
Enclosure
5
respond to a loss of normal electrical power to its associated safety bus. This finding
was assessed using IMC 0609. Appendix A and preliminarily determined to be White
(low to moderate safety significance) based upon a Phase 3 Risk Analysis with an
exposure time of 323 days which resulted in a total (internal and external contributions)
calculated conditional core damage frequency (CCDF) of 7.1 E-6. The cause of this
finding is related to the crosscutting area of Human Performance, Resources aspect
H.2(a} because preventive maintenance procedures for the EDGs were not properly
established and implemented to maintain long term plant safety by maintenance of
design margins and minimization of long standing equipment issues. (Section 2.2)
- ~: The team identified a NCVof 10 CFR 50, Appendix B, Criterion XVI. "Corrective
Action," because Constellation did not thoroughly evaluate and correct a degraded
condition of a C0-8 relay disc sticking or binding issues which can adversely impact the
function of the EDGs and the electrical distribution protection scheme. Specifically,
following the February 18. 2010 event, Constellation did not identify and adequately
evaluate the recent CO*8 relay failures due to sticking or binding of the induction discs in
the safety related and non-safety related applications. Constellation entered this issue
into the corrective action program (CR 20100004673).
The finding is more than minor because it is associated with the equipment reliability
attribute of the Mitigating Systems Cornerstone, and it adversely affected the associated
cornerstone objective of ensuring the availability. reliability, and capability of systems
that respond to initiating events to prevent undesirable consequences (I.e., core
damage). This finding was determined to be of very low safety significance because
these historical relay failures did not result in an actual loss of system safety function.
The cause of the finding is related to the crosscutting area of Problem Identification and
Resolution, Corrective Action Program aspect P.1(c) because Constellation did not
thoroughly evaluate the previous station operating experience of CO-8 relay induction
disc sticking and binding issues such that resolutions addressed the causes and extent
of-condition. (Section 2.3)
- Green: A self-revealing NCV of Technical Specification (TS) 5.4.1.a, "Procedures" was
identified for failure to establish adequate procedures for restoration of Chemical and
Volume Control System (CVCS) letdown flow. On February 18, 2010, an electrical
ground fault caused a Unit 1 reactor trip, loss of the 500 kV Red Bus, and cves letdown
isolation as expected on the ensuing instrument bus 1Y10 electrical transient. Deficient
operating instructions prevented timely restoration of letdown flow following the initial
transient. Pressurizer level remained above the range specified in Emergency
Operating Procedure (EOP}-1 for an extended period because of the operators' inability
to relstore letdown. This ultimately led to exceeding the TS high limit for pressurizer
level. CVCS Operating Instruction Ol-2A was subsequently revised, providing
necessary guidance for re-opening the letdown system excess flow check valve to
restore letdown flow. This event was entered into the licensee's corrective action
program (CR 2010-001378).
The finding is more than minor because it is associated with the procedure quality
attrilJute of the Mitigating Systems Cornerstone and affected the cornerstone objective to
ensure the availability, reliability, and capability of systems that respond to initiating
events to prevent undesirable consequences (Le., core damage). The finding is of very
low safety significance because it is not a deSign or qualification deficiency, did not
represent a loss of a safety function of a system or a Single train greater than its TS
Enclosure
6
allowed outage time, and did not screen as potentially risk significant due to external
events. This finding has a crosscutting aspect in the area of human petiormance,
resources aspect H.2(c), because Constellation did not ensure that procedures for
restoring eves letdown were complete and accurate. (Section 3.1)
Enclosure
7
REPORT DETAILS
1.
Background and Description of Events
In accordance with the Special Inspection Team (SIT) charter (Attachment 2), team
members (the team) conducted a detailed review of the February 18, 2010, dual unit trip
with complications at Calvert Cliffs Nuclear Power Plant including equipment and
operator response. The team gathered information from the plant process computer
(PPC) alarm printouts, interviewed station personnel, performed physical walkdowns of
plant equipment, and reviewed procedures, maintenance records, and various technical
documents to develop a detailed timeline of the event (Attachment 3). The following
represents an abbreviated summary of the Significant automatic plant and operator
responses which began at 8:24 a.m. on February 18, 2010, and ended on February 22,
2010, with both Unit 1 and Unit 2 in cold shutdown:
On February 18, 2010, at 8:24 a.m., the Unit 1 reactor automatically tripped from 93
percent reactor power in response to a reactor coolant system (RCS) low flow condition.
Water had leaked through the auxiliary building roof into the 45' elevation switchgear
room, causing an electrical ground on bus 14 which tripped the 12B reactor coolant pump
(RCP), thereby initiating the reactor protection system trip on RCS low flow. Three of the
four Unit 1 RCPs continued operating.
Ground overcurrent (O/C) relay 2RY251 G/B-22-2 failed to actuate as designed,
permitting the Unit 1 ground O/C condition to reach the Unit 2 2213 kV RCP bus and the
associated 500 kVl13 kV transformer (P-13000-2). Ground O/C protection for the P
13000-2 transformer actuated which deenergized the 500 kV "Red Bus" offsite power
supply. the 22 bus, and all four RCPs. At 8:24 a.m., the Unit 2 reactor automatically
tripped from full reactor power in response to the associated reactor protection system
trip on ReS low flow.
The P~13000-2 isolation also deenergized the 21 13 kV service bus, which deenergized
the Unit 1 144 kV safety bus, the Unit 2 24 4 kV safety bus, and several Unit 2 non
safety related 4 kV busses. The 16 emergency diesel generator (EDG) started as
designed and reenergized the Unit 1 14 bus. The 26 EDG started. but tripped 15
seconds later due to a low lube oil pressure signal and the 24 bus remained deenergized.
The electrical transient deenergized 120 volt instrument buses 1 Y1 0 and 2Y10. which
isolated the chemical volume control system (CVCS) and ~CS letdown for both units and
. complicated operators' control of pressurizer level.
Loss of power to the Unit 2 non-safety related buses resulted in loss of the normal RCS
heat removal path (main feedwater pumps, circulating water pumps, and condenser).
Operators used the turbine driven auxiliary feedwater pump and atmospheric steam
dump valves for decay heat removal.
At 8:48 a.m., Unit 2 operators exited emergency operating procedure (EOP)-O. "Reactor
Trip" and entered EOP-2, "Loss of Flow and Loss of Offsite Power." At 8:57 a.m.,
operators reenergized the 24 bus via the altemate feeder breaker. At 9;00 a.m., Unit 2
operators restored RCS letdown and maintained appropriate pressurizer level control.
At 1'I :17 a.m., Unit 2 operators started the 23 motor driven auxiliary feedwater (AFW)
pump and secured the turbine driven AFW pump. At 11:18 a.m., Unit 2 operators exited
Enclosure
8
the EOPs and returned to normal operating procedures. As of 12:02 p.m., Unit 1
Operl:ltors remained unsuccessful at restoring RCS letdown and exceeded the
pressurizer high level limits specified by both EOPs and TS. At 1 :09 p.m., Unit 1
operators restored RCS letdown and restored normal pressurizer level control. At 1 :38
p.m., Unit 1 operators exited the EOPs and returned to normal operating procedures.
At 2:07 p.m., Unit 1 vital 4 kV bus 14 was aligned to its alternate offsite source and the
18 EDG was secured. At 5:13 p.m., Unit 2 operators started 21B and 22A RCPs to
restore forced RCS circulation. On February 19, 2010, at 12:05 p.m., operators verified
two offsite power supplies were available, with the 21 13 kV service bus energized from
an alternate offsite source. On February 20,2010, at 10:31 p.m. repairs on the 2B EDG
were completed and the diesel generator was declared operable.
Unit 1 achieved cold shutdown at 5:38 a.m. on February 21, 2010, and 500 kV Red Bus
was restored at 5:50 a.m. Unit 2 achieved cold shutdown at 5:00 a.m. on February 22,
2010.
2.
Equipment Performance
2.1
Untimely Corrective Actions to Unit 1 45 Foot Elevation Switchgear Room Roof Leak
Cam,ed Reactor Trip
a.
Inspection Scope
Water leakage through the Unit 1 auxiliary building roof into the 45' elevation switchgear
room, caused an electrical ground on Bus 14 which tripped the 12B RCP, thereby
initiating a reactor protection system trip on RCS low flow. The team interviewed station
personnel, performed field walkdowns, and reviewed various records including
maintenance backlogs, maintenance history, operating logs, condition reports, and
maintenance rule program records to independently determine the cause of the event
and assess associated corrective actions. Constellation determined the root cause ot
the e:vent was that Calvert Cliffs lacked sensitivity to the consequences associated with
degr;sded roof conditions which led to a reactive rather than preventive strategy for
dealing with roof leaks. The team independently reviewed Constellation's Root Cause
Analysis Report (RCAR) for the Unit 1 reactor trip to determine the adequacy of the
evaluation, the extent-ot-condition review, and associated corrective actions.
b.
Findings
Introduction: A self-revealing non-cited violation (NCV) of very low safety significance
associated with 10 CFR Part 50, Appendix B, Criterion XVI "Corrective Actions," was
identified because Constellation did not promptly identify and correct degraded
conditions associated with the Unit 1 auxiliary building (45-foot elevation switchgear,
room) roof leakage. These degraded conditions led to the failure of the auxiliary building
to provide adequate protection to numerous safety related systems from external events
(adverse weather conditions) resulting in a ground on a reactor coolant pump (RCP) bus
and a consequential Unit 1 reactor trip on February 18, 2010.
Description: On February 18, 2010, Unit 1 tripped due to water from a roof leak entering
into the Unit 1 45-foot elevation switchgear (SWGR) room and causing a phase to
ground short near a current transformer (CT) for the 12B RCP bus 14P
Enclosure
9
differential/ground current protection devices. The ground fault was not isolated close to
the source, due to a failed ground protection relay in the feeder breaker to the Unit 1
RCP bus. The consequential trip of the 12B RCP led to the Unit 1 reactor protection
system (RPS) trip due to the a low reactor coolant system (RCS) flow signal.
While conducting a review of the dual unit trip, the team noted that in July of 2008,
condition report (CR) IRE-032-766 was written regarding rain water which had fallen onto
and into the emergency shutdown panel (ESOP) 1 C43, which is located in the Unit 1 45'
elevation SWGR room. Immediate actions were taken to notify the control room
supervisor of the condition as well as to clean up the pooled water around the panel.
Corrective actions were initiated to establish a program to maintain weather tight building
integrity. In June of 2009, CR 2009-004060 documented water dripping inside the
SWGR room just east of the No. 12 motor generator set. No immediate actions were
taken; however, recommended actions were to repair the roof. On August 8, 2009, a .
third CR (CR 2009-005508) was written, again regarding water leaking into the SWGR
room and onto the ESOP. Immediate actions were taken to cover the panel with
herculite and to direct the leaking water into a plastic bucket, as well as mopping up the
standing water. Despite the immediate actions taken to address the three rain water
issues, no additional actions were taken to properly prioritize, identify, and correct the
roof leakage. This is evident due to the fact that each CR was given the lowest priority
(category 4) as well as none of the work orders written to address the roof leakage* had
been approved. Additional safety related SWGR equipment in the SWGR room included
power supply breakers for the "B" train auxiliary feed water pump, high pressure safety
injection pump, low pressure safety injection pump and EDG.
, Based on the review of the RCAR, the team noted several missed opportunities from
2002 to 2009 to identify and evaluate the degraded condition prior to the dual unit trip.
During a periodic bus inspection in 2004, repairs were made to insulating material on the
power cables inSide the 14P01 cubicle to correct a water spot on the "B" phase of the
12B RCP bus. This cubicle is in the same SWGR enclosure as the 14P02 cubicle where
the water intrusion occurred that resulted in the February 18, 2010 trip. The work was
completed under the bus inspection work order; however, no CR was written
documenting the indicated water intrusion. This preventive maintenance activity should
have led to an investigation into the cause of the water intrusion as well as the extent of
the degraded condition. An apparent cause (IRE-007-705) was also completed in 2005
in response to a CR written by quality assurance personnel noting that there were 33
leaks identified during a walk down but no trend CR was written. Corrective actions were
proposed; however they were not adequately implemented.
The Calvert Cliffs' maintenance rule scoping document states that the function of the
auxiliary building is to provide structural support and separation to safety and non-safety
relatE~d equipment while accounting for the effects of certain extemal events. Rain
storms and heavy snowfall are eKamples of external events for which the auxiliary
building is designed to provide protection against. The Calvert Cliffs' structure
monitoring program did not effectively use the corrective action process to ensure this
function of the auxiliary building would be maintained. At the time of this special
inspe:ction, 58 work orders were open to repair roof leaks. None of these work orders
were planned or scheduled. Several of these work orders were over 2 years old.
Immediate corrective actions included: repairing degraded areas of the auxiliary building
roof; performing walk downs of other protected area buildings that could be susceptible
Enclosure
I
10
to damage to electrical equipment due to water intrusion; issuing standing orders to
include guidance regarding prioritizing work or.ders due to roof leakage; and identifying
furthE~r actions to take during periods of snow or rain to ensure plant equipment is not
affected. Long-term corrective actions include implementing improved plant processes
for categorization, prioritization, and management of degraded roof and water leakage
issues.
The team concluded that Constellation had numerous opportunities to have thoroughly
evaluated, classified, and prioritized the roof leakage, such that corrective actions could
have addressed the full extent of the auxiliary building roofing degraded condition and
prevented the water intrusion event and subsequent plant trip on February 18,2010.
. The team concluded that station personnel did not properly inspect and maintain the
roofs of several safety related structures to ensure the internal safety related and non
safety related components were protected from effects of the external environment (Le.,
rain, snow).
Analysis: The failure of Constellation to promptly identify and correct conditions adverse
to quality, associated with the auxiliary building roof leakage. is a performance
deficiency. The finding is more than minor because it is associated with the Initiating
Events Cornerstone and affects the cornerstone objective to limit the likelihood of those
external events that upset plant stability and challenge critical safety functions during
shutdown, as well as power operations. The inspectors evaluated this finding using IMe
0612 Attachment 4, "Phase 1- Initial Screening and Characterization of Findings," The
team determined the finding to have very low safety significance because, although it
contributed to a reactor trip, it did not contribute to the likelihood that mitigation
equipment would not be availab!e.
The cause of this finding is related to the Problem Identification and Resolution cross
cutting area. corrective action program, because Constellation did not thoroughly
evaluate the problems related to the water intrusion into the-auxiliary building such that
the resolutions addressed the causes and extent-of-condition. This included properly
classifying, prioritizing. and evaluating the condition adverse to quality (P.1{c)).
Enforcement: 10 CFR Part 50, Appendix B. Criterion XVI "Corrective Action," states, in
part, that conditions adverse to quality, such as failures, malfunctions, deficiencies,
deviations, defective material and equipment, and non-conformances are promptly
. identified and corrected. Contrary to the above, from 2002 to February 18. 2010,
Constellation did not thoroughly evaluate and promptly correct degraded conditions
associated with auxiliary building roof leakage. This led to the failure of the auxiliary
building to provide protection to several safety related systems from external events (Le.
flooding), a ground on a reactor coolant pump bus, and ultimately a Unit 1 reactor trip.
Beccluse this violation was of very low safety significance and was entered into the
licensee's corrective action program as CR 2010-001351, this violation is being treated
as an NCV, consistent with the NRC Enforcement Policy." (NCV 0500317/318/2010006
01: Failure to Thoroughly Evaluate and Correct Degraded Conditions Associated
with Auxiliary Building Roof Leakage)
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Enclosure
11
2.2
Deficient Preventive Maintenance Program Procedures and Implementation for EDG
Aqastat Time Delay (TO) Relays
.
a.
InspE3ction Scope
On February 18, 2010, Unit 2 experienced an automatic reactor trip, loss of the P-13000
2 Service Transformer, and loss of the 500 kV Red Switchyard Bus. The loss of the Red
Bus resulted in loss of power to the No. 244 kV safety bus which caused an automatic
start of the 2B EDG. The 28 EDG tripped due to low lube oil (LO) pressure after running
for 15.2 seconds. The team reviewed the timing sequence, design requirements, relay
schematics, and surveillance and maintenance history for the 2B EDG. Failure of a T3A
time delay (TD) relay coincident with the 28 EDG LO low pressure protection logic not
having reset caused the low LO pressure protective trip of the engine. Constellation
identified two root causes for the EDG failure: (1) station personnel failed to recognize
and quantify the low margin in all aspects of the low lube oil.pressure trip set feature for
the EDG; and, {2} station personnel did not rigorously assess all failure modes of the
Agastat relays in the EDG protection circuitry prior to extending its service life beyond
the vendor qualified life.
The team reviewed Constellation's evaluation of the 28 EDG's failure, the adequacy of
proposed and completed corrective actions, and the appropriateness of the extent-of
condition review. Independent reviews of design documents, mock-Up testing. drawings,
surveillance testing, and field walk-downs were performed by the team to evaluate the
cause of the 2B EDG failure. In addition, the team reviewed Constellation's preventive
maintenance (PM) history and associated PM programs.
b.
Findings
Introduction. The NRC identified an apparent violation of Technical Specification 5.4.1
for the failure of Constellation to establish, implement, and maintain preventive
maintenance requirements associated with safety related relays. The team identified
that Constellation did not implement a performance monitoring program in lieu of a
previously established 10-year service life replacement PM requirement for the 2B EDG
T3A TD relay. As a consequence, the 2B EDG failed to run following a demand start
signal on February 18, 2010. This apparent violation is preliminarily determined to be of
low-to-moderate safety Significance {White}.
Description. The purpose of the T3A (Agastat 7000 series) TD relay in the EDG
protective circuit is to bypass the low lube oil trip on the EDG start to allow the EDG lube
oil pressure to initially build up to operating conditions. The relay begins timing when the
EDG speed reaches 810 rpm (approximately 6 seconds after EDG start). The relay
functions to bypass the low LO pressure trip <<17 pounds pressure sensed in the EDG
upper crankcase) for 15 seconds (a total of 21 seconds from EDG start). This time delay
allows LO pressure to build-up in the EDG upper crankcase high enough to reset the trip
logic (2 of 3 pressure switches reset at >20 pounds). The Unit 2 February 18, 2010,
sequence of events printout revealed that the T3A relay timed out early (after 9.2
seconds) at 15.2 seconds following the EDG start and prior to the low LO pressure
sensing trip logic being reset. Constellation determined that a typical fast, non-pre
lubricated EDG start results in LO pressure exceeding 20 pounds pressure
approximately 13 seconds following the start of the EDG. Accordingly, the early timeout
Enclosure
12
of the T3A relay was not the only degraded 28 EDG condition that presented itself on
February 18, 2010. Constellation attributed the February 18 delayed reset of the
pressure switches to "sticky lubrication oil" in the %-inch stainless steel pressure sensing
line to the pressure switches, vice an actual low LO pressure condition in the diesel
engine upper crankcase.
The team determined that the T3A relay, which timed-out early, had been in-service on
the 28 EDG for approximately 13.5 years, 3.5 years beyond its vendor recommended
10-year service life. In 2001, Constellation engineering discontinued the vendor
recommended 10-year replacement PM and substituted a performance monitoring
program envisioned to ensure Agastat relays (approximately 100 safety related
applications and 500 to 600 non-safety related applications in the two Calvert Cliffs units)
were appropriately monitored and replaced prior to failure (reference Engineering
Service Package ESP No. ES200100067, approved 03/06/2001). The team identified
that a relay performance monitoring program had not been establiShed since 2001 at
Calvert Cliffs. Constellation initiated CR 2010-04493 to address this performance issue.
The Shift Manager reviewed the immediate operability and determined that the other
safety-related components using Agastat relays remain operable because these relays
are installed in less harsh operational environments (e.g. vibrations) then the EDG
Agastat relays, and therefore, are less susceptible to age-related degradation. In
addition, CR 2010-01784 was written to address the extent-ot-condition of Agastat relays
used in other safety-related applications.
Constellation replaced the 28 EDG failed T3A relay and, via a single 'as-found' bench
test, validated its February 18, 2010, in-service failure, when the relay failed again,
timing out early at 11.6 seconds. Subsequent attempts by Constellation to adjust the
relay to within calibration tolerance were unsuccessful. The failed relay was shipped to
an independent laboratory for diagnostic testing and destructive examination. The
laboratory identified that, exercised over its furl range of operation, >40 percent of the TD
actuation results were out of tolerance. Internals examination identified three of six
screws on the flexible diaphragm retaining ring were loose, suggesting that the early
time-out of the relay was possibly due to excessive air bleed off (leakage passed the
diaphragm seal). Constellation concluded that the TD relay failure was a relatively
recent event (within the last 47 days) and attributable to the three 28 EDG starts and
approximately seven cumulative hours of operation that occurred in early January 2010.
The team concluded that Constellation provided no evidence to support the approximate
time of failure of the TD relay. However, the team determined that the failure and
probable failure mechanism may have occurred between the last successful calibration
of the TD relay (May 13,2008) and the observed failure on February 18,2010. In
addition, the team conCluded that therD relay early time-out was most likely a latent
failUre and masked by the monthly EDG surveillance test. Accordingly, the TD relay
failure was revealed by the fast, non-pre-Iubrication, demand start on February 18, 2010.
The basis for the team's conclUSion was as follows:
- Constellation'S troubleshooting results were not conclusive regarding the lubricating
oil pressure sensing line "'sticky oil" theory, based upon the following: 1} the "sticky
oil" drained from the sensing line was not saved or analyzed for consistency or
contaminants (Constellation did not exercise appropriate quarantine practices); 2) the
%-inch LO pressure sensing line was not backfilled with oil and was therefore
susceptible to trapped air pockets that may tend to dampen accurate pressure
Enclosure
13
sensing and may result in a delayed pressure response; and, 3) Constellation's
routine (two-year calibration cycle) and post-event calibration checks of the pressure
switches did not record "as-found" values of the pressure switch reset values; this
information may have assisted in ruling out possible pressure switch setpoint drift or
malfunction.
The team acknowledged that Constellation's subsequent mock-up testing of the
pressure sensing line did show that lubricating oils of heavier viscosity tend to delay
the pressure sensing response. However, the 100W oil used to demonstrate the
phenomena (approximate 3 second pressure sensing delay) was considerably
heavier than the lubricating oil used in the 2B EDG {40W} and mayor may not have
re!flected the "sticky oil" viscosity observed by the technician responsible for the
pressure switch troubleshooting.
- The fast, non-pre-Iube start of the 2B EOG contributed to the identification of the
failed relay; whereas the monthly pre-lube EDG starts likely masked the failure of the
TO relay. The team determined that for a typical fast, pre-lubricated EOG start, a
small pre-lube pump is run for 3 to 5 minutes prior to the EDG starting and fills the
upper crankcase with lubricating oil, but is not of sufficient capacity to pressurize the
upper crankcase. When the EOG starts, the engine driven LO pump functions to
complete the upper crankcase fill and pressurization (>20 pounds pressure) in
approximately 8 seconds. Accordingly, any relay failure (timing out early, <12
s,~conds) is masked by the fast, pre-lube EDG start because the relay actuates at 6
seconds and only has to satisfactorily function (block the low lube oil trip signal) for >2
seconds. The team noted that by the low LO pressure protective system design. the
fast pre-lube EOG starts allow for a significant margin to satisfactory build-up of lube
all pressure before the TO relay times out (a margin of approximately 13 seconds).
For the fast non-pre-Iube start, LO pressure typically exceeds 20 pounds pressure at
13 seconds after EDG start. This 13 second time interval similarly translates to the
TD relay having to function for >7 seconds from the time it actuates at 6 seconds from
EOG start. This 7 seconds minimal TO function also, by design, provides margin (an
additional 8 seconds) for satisfactory LO pressure bUild-Up.
The team concluded that the last known satisfactory relay calibration (setpolnt) check of
the T3A relay was the two-year calibration check completed on May 13, 2008. Based
upon Constellation records, the as-found setting was 17.5 seconds and the as-left was
16.5 seconds. All monthly surveillance tests of the 2B EDG since May 13, 2008, were
fast, pre-lube starts. There were no demand starts of the 2B EDG between May 13,
2008, and February 18, 2010, that would have proved or disproved that the T3A relay
was operable, and that the LO pressure senSing line issue was coincidental or
precipitous of a fast, non-pre-Iube start.
Following identification of the failed T3A relay. the licensee replaced the relay,
satisfactorily tested the 2B EDG, and returned the 2B EOG to service. In addition, time
delay relays used in the 1 B* and 2A EDG protective circuits, that also exceeded the
vendor recommended 10-year service life, were replaced. Constellation is evaluating the
continued use of Agastat relays beyond their vendor recommended 10-yr service life. As
previously noted, there are approximately 100 safety related applications and 500-600
non-safety related applications at the two Calvert Cliffs units.
Enclosure
14
Analysis. The team identified that the failure of Constellation to perform preventive
maintenance in accordance with vendor recommendations without adequate
performance monitoring on safety related Agastat 7000 series TO relays used in safety
relat~~d applications is a performance deficiency and violation of Technical Specifications
(TS). This violation of TS is more than minor because it is associated with the
equipment performance attribute of the Mitigating Systems Cornerstone and adversely
impacted the objective of ensuring the availability, reliability, and capability of systems
that respond to initiating events to prevent undesirable consequences. Specifically, the
early timeout of the T3A relay caused the 2B EDG to trip prior to the low lube oil
pressure trip signal clearing (resetting) after a demand fast start on February 18, 2010.
The failure of the 2B EDG to run resulted in the continued loss of alternating current to
the No. 24 4 kV safeguards bus and its associated emergency core cooling systems.
In ac~cordance with Table 4a of IMC 0609, Attachment 04, "Phase 1
Initial Screening
and Characterization of Findings," this performance deficiency required a Phase 2 or 3
risk analysis because the issue resulted in an actual loss of safety function of a single
train for greater than its TS allowed outage time. A Phase 3 risk assessment was
perfc)rmed by a Region I Senior Reactor Analyst (SRA) using the SAPHIRE software and
Calvert Cliffs Unit 2 Standardized Plant Analysis Risk (SPAR) model, Revision 3.46,
dated February 2010.
To conduct the Phase 3 analysis, the SRA made the following modeling assumptions;
Exposure time was based upon a T/2 approximation. The team determined that
the 2B EDG exposure time is best approximated by a T/2 value, per the usage
rules of IMC 0308, Appendix A, "Technical Basis for At Power Significance
Determination Process." Specifically, if the inception of a condition is unknown,
the use of the mean exposure time (T/2) is a statistically valid time period
because it represents one-half of the time since the last successful demonstration
of the component's function and the time of discovery or known failure. The last
successful demonstration of the T3A relay was the calibration check performed
on May 13, 2008. The total time (T) between May 13, 2008 and February 18,
2010 is 646 days. Therefore, T/2 represents an approximate exposure time of
323 days or 7752 hours0.0897 days <br />2.153 hours <br />0.0128 weeks <br />0.00295 months <br />.
SPAR model basic event EPS-DGN-FS-2B, representing "Diesel Generator 2B
Failure to Start" was set to TRUE. The basis for the TRUE. vice a failure
probability of 1.0, is that common cause failure of the remaining Fairbanks-Morris
EDGs could not be conclusively ruled out. The same type Agastat 7000 series
TD relays, with comparable greater than 10 years in-service times were installed
on the 1Band 2A EDGs.
SPAR model basic event AFW-XHE-XM-FC8, representing operator failure to
open the Turbine Building to turbine driven auxiliary feed water (TDAFW) pump
room door within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> of a station blackout event, was set to FALSE. The
basis for this change is that recent engineering analysis of the TDAFW pump
room heat-up (post Appendix R fire, LOOP/LOCA, SBO) identified no
dependency on operator action to open the door to the turbine building to ensure
adequate cooling of the TDAFW pumps.
Enclosure
15
No additional 2B EDG recovery credit was applied to the model based upon this
event. The SRA noted that 2B EDG non-recovery probability (0.772) in the SPAR
model is based upon industry statistical data. The SRA notes that Constellation
procedures have operators align the OC EDG (within 45 minutes) vice attempt to
troubleshoot and restart the failed EDG. Accordingly, any subsequent attempts
to restart the 2B EDG. after an approximate one hour delay (aligning the OC
EDG) would likely have the same result because all LO would have drained from
the upper crankcase.
Even though Agastat 7000 series relays are used in multiple safety related
applications (some beyond their vendor recommended service life), no broad
based increase in safety related systems' or components' failure probabilities was
applied for this Phase 3 risk assessment. As a consequence, the calculated risk
estimate for this condition may be a non-conservative value because the Agastat
relays are used in multiple other safety related applications beyond the
manufacturers recommended 1 O-year service life.
Truncation for the SPAR model analysis was set at 1E-13.
USing the above stated assumptions. the increase in internal risk (core damage
frequency) associated with the 2B EDG failure of February 18, 2010, was estimated at
6.DE-6. The dominant core damage sequence involves the loss of Facility B (13 kV
Service Bus No. 21), loss of steam generator cooling (main feedwater and auxiliary
feedwater), and the subsequent loss of once through cooling (feed and bleed. using the
charging system and a power operated relief valve).
Base!d upon the absence of an NRC external risk quantification tool, the SRA used
Constellation's ca[culated extemal risk values to approximate the external risk
contribution. Constel!ation's estimated external risk is based. upon a RISKMAN fire
modeling tool and was calculated at 1.1 E-6 for the T/2 exposure period. No appreciable
external risk contributions were identified for flooding or seismic events. The dominant
core damage external events include turbine building fires (involving the steam generator
main feedwater pump area) and high wind/hurricane events. The dominant turbine
building fire scenarios involve the failure of the available EDGs (2B and 1 B) and a
spurious initiation of the safety feature actuation system (SFAS). The dominant high
wind/hurricane event core damage scenarios involve the assumed failure of the OC
EDG. the subsequent failure of the remaining safety related EDGs, and a spurious
SFAS.
Based upon the SRA's calculated internal events risk estimate and Constellation's
estimated external events risk contribution, the total increase in Unit 2 core damage
frequency for this finding is approximately 7.1 E-6. Accordingly, this finding is of low to
modlarated safety significance (WHITE). This finding and the associated risk analysis
was reviewed by a Significance and Enforcement Review Panel (SERP) conducted on
June 1,2010. The SERP concluded that the stated Technical SpeCification violation and
associated risk characterization were appropriate. The violation does not represent an
immediate safety concern because the licensee took prompt corrective actions to
replace the Agastat relays in use beyond their service life for an three Fairbanks-Morris
EDGs and ensured the LO pressure sensing lines were properly backfilled. Subsequent
testing of all three EDGS verified operability, including a non-pre-Iubricated fast start of
the 2B EDG.
Enclosure
16
The Constellation PRA staff performed a risk assessment of the 2B EDG failure using
their CAFTA internal events model and RISKMAN external events model. Constellation
assumed the same exposure time as the Region I SRA of T/2 equal to 323 days.
Constellation's total risk estimate was 3.1 E-6 CDF. Based upon discussions with the
Constellation PRA staff, their risk estimate and dominant core damage sequences
compare favorably with the NRC results.
The cause of this finding is related to the crosscutting area of Human Performance,
I*
resources aspect because preventive maintenance procedures for the EDGs were not
properly established and implemented to maintain long term plant safety by maintenance
of design margins and minimization of long standing equipment issues (H.2(a).
Enforcement. Technical Specification 5.4.1 states, in part. that written procedures
I
specified in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978, shall be
I* !
established, implemented, and maintained. Section 9.b. of Appendix A to Regulatory
Guide 1.33 states, in part, that preventive maintenance schedules should be developed
to specify replacement of parts that have a specific service life. In March 2001
I
Constellation replaced their original10-year relay replacement preventive maintenance
with a proposed performance monitoring program, to ensure the continued reliability and
I
!
operability of Agastat relays installed in safety related applications beyond the vendor
recommended 10-year service life, via Engineering Change Package No. ES200100067.
Contrary to the above, the team identified that Constellation did not establish a
performance monitoring program, and aU Agastat relays installed in safety related
applications at Calvert Cliffs have been subject to "run to failure" preventive
maintenance/replacement interval. Constellation took prompt corrective action to
replace Agastat relays used in service, beyond their 10-year service life, in the 2B, 2A
and 1 B EDGs. The remaining Agastat relays, used in safety related applications beyond
their vendor recommended service life, are under evaluation by Constellation.
Constellation has initiated several CRs (see Attachment 1 to this report) associated with
this performance deficiency. Pending final significance determination, the finding is
identified as Apparent Violation (AV)05000318/2010006-02, Inadequate Preventive
Maintenance Results in the Failure of the 28 Emergency Diesel Generator.
2.3
Ground Fault Relay 251 G/B-22-2 Did Not Actuate on Ground Overcurrent to Trip Open
Breaker 252-2202
a.
Inspection Scope
The team reviewed design requirements, drawings, and maintenance history of the
251 GfB-22-2 relay. Failure of this relay to actuate and trip open the 252-2202 breaker
resulted in a loss of the P-13000-2 service transformer, which resulted in loss of power to
the Unit 2 RCPs and a Unit 2 trip with loss of normal decay heat removal. Unit 2
remained on atmospheric dump valves and auxiliary feedwater for heat removal for
approximately 68 hours7.87037e-4 days <br />0.0189 hours <br />1.124339e-4 weeks <br />2.5874e-5 months <br />. Constellation determined the most likely cause of the relay
failUre was premature coil aging due to the operating environment and the magnitude of
the current seen, which caused insulation breakdown and shorting of the magnetizing
coil. Even though Constellation could not conclusively identify the cause of the insulation
breakdown and magnitude of the signal that coincided with the breakdown, they did note
that the relay in this particular application is located in non-environmentally controlled
Enclosure
17
space which would impact aging mechanisms due to the temperature extremes.
Additionally, the 251 G/B-22-2 relay age was 39 years at the time of tlie event, which is
only 1 year within the 40-60 year service life.
The team reviewed Constellation's root cause analysis report (RCAR) for the 251 G/B-22
2 relay to determine the adequacy of the evaluation and the appropriateness of the
extent-of-condition review. Independent reviews of the design documentation, drawings,
maintenance history, and field walk-downs were performed to validate the cause of the
relay failure. The team reviewed the design requirement and the relay setting
information of the 13.8 kV fault protection relaying scheme to ensure proper equipment
protection during transient and steady state conditions. The team also reviewed the
history of the 251G/B-22-2 relay, along with other protective relays in the 13.S kV system
that were required during the event, to verify that the applicable test acceptance criteria
and maintenance frequency requirements were met.
b.
Findings
DefiGient Evaluation and Untimely Corrective Action Associated with Induction Disc
Bincling on CO-8 Type Relays
Introduction: The team identified a finding of very low safety significance (Green) that
involved a NCVof 10 CFR 50, Appendix B, Criterion XVI, "Corrective Action," because
Constellation did not thoroughly evaluate and correct a degraded condition of CO-S relay
disc sticking or binding issues which can adversely impact the function of the EDGs and
the electrical distribution protection scheme. Specifically, following the February 18,
2010, event Constellation did not identify and adequately evaluate the recent CO-S relay
failures due to sticking or binding of the induction discs in the safety related and non
safety related applications.
Description: The team reviewed Constellation's RCAR for the relay 2RY251 G/B-22-2 on
breaker 2BKR252-2202 which failed to trip open the breaker. The relay was a CO-S
ground fault over-current relay which had been in service for the life of the plant. The
relay consists of an electromagnet and an induction disc which rotates to close a moving
contact to a stationary contact to complete the breaker trip circuitry. The root cause
analYSis concluded that the magnetizing coil had shorted out the majority of the windings
in a manner that current would pass but the induction disc would not rotate.
The team reviewed Constellation's maintenance and corrective action history of the CO
S relay failures and noted that the induction disc type relays had a failure history
aSSOCiated with disc binding and sticking conditions. The team also noted that CO-S
relays and other induction disc type relays had a high failure rate for out of tolerance
conditions during the performance of relays calibration procedures. The team
determined that failures of the relay due to binding, sticking, and out of tolerance
conditions can potentially impact the breaker trip operation and affect breaker
coordination.
The failure history for binding, sticking, and out of tolerance conditions for the induction
type relays were reviewed since 2007. The team found 40 failures since 2007 and 5
failures of the CO-8 type relays. Constellation has a total of 68 CO-S type relays
installed in safety related and non-safety related applications, all of which have been
SChE~duled to be calibrated every 2 years since 2005. The team noted that from 1999 to
Enclosure
18
2005 as-found testing and calibration of the relays were performed every 4 years. The
team reviewed the failure data of the CO-8 and other induction disc type relays prior to
2005 and concluded that the failure rate did not change significantly subsequent to the
increase in calibration frequency. The CO-8 relay failures were noted to be 10 percent
from 1999-2005.
Constellation replaced or cleaned the relays with sticking or binding conditions; however,
the licensee did not place the relays in any system or component monitoring program.
The relays were also not part of the system health tracking report. The team reviewed
the historical failures of the CO-8 relays and noted that for some of the testing
conditions, the induction disc needed to be mechanically agitated to free it from the
binding or sticking conditions. The team reviewed the vendor and Electric Power
Research Institute (EPRI) calibration and maintenance manual and determined that
Constellations' calibration and inspection procedure did not include all of the
recommended practices specified in the EPRI guideline related to inspection and
cleaning of the induction disc units. Constellation entered this issue into the corrective
action program (CRs 2010-004672 and 2010-004673).
Ana~ysis: The team reviewed Constellation's root cause evaluation, which concluded the
cause of the relay failure to be premature coil aging due to its operating environment and
the magnitude of the current seen by the relay. The team concluded that there was no
direct correlation between the coil failure and the historical binding and sticking
conditions of the C0-8 relay discs. However the team determined that Constellation's
failure histories ofthe CO-8 type relays were significant and the failure to evaluate the
degraded conditions and implement timely and effective action to correct this condition
adverse to quality was a performance deficiency. The CO-8 relays are used in multiple
safety related and non-safety related applications.
The finding was more than minor, in accordance with NRC IMC 0612, Appendix B,
"Issue Screening," (lMC 0612B) because, while it was not similar to any examples in IMC 0612, Appendix E, "Examples of Minor Issues" (IMC 0612E), it was aSSOCiated with the
equipment reliability attribute of the Mitigating Cornerstone and it adversely affected the
ass()ciated cornerstone objective of ensuring the availability, reliability. and capability of
systems that respond to initiating events to prevent undesirable consequences (I.e., core
damage). The team evaluated this finding using IMC 0612 Attachment 4, "Phase 1
Initial Screening and Characterization of Findings." The finding is of very low safety
significance (Green) because it is not a design or qualification deficiency, did not
repr<i;~sent a loss of a safety function of a system or a single train greater than its TS
allowed outage time, and did not screen as potentially risk significant due to external
events. The historical relay failures did not result in an actual loss of system safety
function.
The cause of the finding is related to the crosscutting area of Problem Identification and
Rest::Jlution, Corrective Action Program because Constellation did not thoroughly
evaluate the previous station operating experience of CO-8 relay induction disc sticking
and binding issues such that resolutions addressed the causes and extent-of-condition
(P.1(c>>.
Enfmcement: 10 CFR 50 Appendix B, Criterion XVI, "Corrective Action," requires. in
part, that measures shall be established to assure that conditions adverse to quality are
promptly identified and corrected. Contrary to the above. Constellation did not
Enclosure
19
adequately evaluate and correct the degraded condition of CO-8 relays which can
potentially impact the function of multiple safety related systems or component. Because
the finding was* of very low safety significance and has been entered into Constellation's
corrective action program (CR 2010-004673), this violation is being treated as a NCV,
consistent with Section VI.A of the NRC Enforcement Policy: NCV 05000317 &
3181:2010006-03, Failure to Evaluate Degraded Conditions Associated With CO-8
Relays and Implement Timely and Effe~ive Action to Correct the Condition
Adverse to Quality.
Deficient Offsite Power Distribution Tripping Scheme Design Control
Introduction: The team identified a finding having very low safety significance (Green)
for failure to translate design calculation setpoint standard listed in calculation E-90-058
and E-90-061 of phase overcurrent relay (250) on feeder breakers 252-1101, 1102,
1103,2101,2102, and 2103 into the actual relay settings.
Description: During the relay settings review, the team identified that the service
transformer 251G/ST-2 and service bus 251G/SB-21 ground overcurrent relays settings
specified in the relay setting sheets did not support the values listed in the relay setting
calculation E-90-61 for the 500/14 kV Service Transformer {P-13000-2}.* The value listed
in the calculations for the 251 G/ST-2 ground overcurrent relay tap settings was 2.5 amps
and the actual field setting, which is set in accordance with the relay setting sheets, was
found to be at 2 amps. For the service bus 251 G/SB-21 the calculation setting of the
time delay value was 4 seconds and the actual field settings was found to be at 3
seconds. Due to these discrepancies Constellation's engineering staff conducted an
evaluation to determine if the actual field settings as specified in the relay setting sheets
for the two overcurrent relays provided adequate coordination to ensure selective
tripping. The relays are designed to detect ground faults on the 13.8 kV system which
have not been cleared by the 500 kV transmission system relays and separate the
station service transformer P-13000-2 from the grid. The team reviewed Constellation's
evaluation and determined that there was no selective tripping coordination impact due
to the relay setting discrepancies on 251 G/ST-2 and 251G/S8-21. However. due to
these discrepanCies identified between the relay setting sheets and the design
calculations, Constellation conducted an extent-ot-condition review for the 13.8 kV
systems to determine it other similar relay settings discrepancies exist.
As a result of the extent-of-condition review, Constellation identified that the phase
overcurrent relay {250} pickup value for the six unit service transformers feeder breakers
252-1101, 1102, 1103, 2101, 2102, and 2103 were set at 1440 amps in accordance with
the relay setting sheets and the values specified in the calculations E-90-058 and E-90
061 were 1200 amps.
The normal system operation deSign when offsite power is available, is the 4.16 kV
system being supplied by the 13.8 kV system through six unit service transformers. The
unit service transformers have overcurrent protection to protect against transformer
faults in the primary or secondary side windings. This overcurrent protection per
calculations E-90-058 and E-90-061 was limited to be at 1200 amps due to the breaker
rating of all of the feeder breakers. Due to the as found relay setting of 1440 amps
exceeding the breaker ratings of 1200 amps, Constellation conducted an operability
analysis and performed a calculation which determined that the maximum load current
possible during the worst case electrical distribution line-up condition would be 982
Enclosure
20
amps. The calculation demonstrated that the maximum load current possible during the
worst case electrical distribution line-up would not challenge the feeder breaker ratings,
and therefore would not cause the breaker to fail prior to the trip operation (tripping).
Analysis: The team determined that the failure to translate the design calculation
setpoint standard values listed in the calculation E-90-058 and E-90-061 of phase
overcurrent relay (250) on feeder breakers 252-1101, 1102, 1103,2101,2102, and 2103
into the actual relay settings was a performance deficiency.
The team determined that this finding was more than minor because it affected the
Initiating Events Cornerstone attribute of equipment performance for ensuring the
availability and reliability of systems to limit the likelihood of those events that upset plant
stability and challenge critical safety functions during shutdown as well as power
operations. Also, this issue was similar to Example 3j of IMC 0612, Appendix E,
"Examples of Minor Issues," because the condition resulted in reasonable doubt of the
operability of the component, and additional analysis was necessary to verify operability.
The failure to translate adequate design calculation setpoint of phase overcurrent relays
on the feeder breakers resulted in an as-found relay setting that exceeded the rating of
the feeder breakers. The team determined that due to the as-found relay setting
exceeding the breaker ratings, certain phase overcurrent conditions could have
potentially caused the breaker to fail prior to the phase overcurrent relay sensing the
degraded condition. The team determined that this condition could affect the recovery of
the safety buses from the electrical grid. The team evaluated this finding using IMC 0612 Attachment 4, "'Phase i-Initial Screening and Characterization of Findings." This
finding was determined to be of very low safety significance (Green) because these
inadElquate relay settings did not result in an actual loss of system safety function and
Constellation also performed an evaluation and determined that the maximum load
current possible would not challenge the feeder breaker ratings. The finding did not
have a cross-cutting aspect because the most significant contributor to the performance
defiCiency was not reflective of current licensee performance.
Enforcement: This finding was not a violation of regulatory requirements because the
unit service transformers and the overcurrent protection relays are not a system or
component covered under 10 CFR Part 50, Appendix B. The issue has been entered
into the licensee's corrective action program (CR 2010-002123. Because this finding
does not involve a violation and has very low safety significance, it is identified as FIN
05000317 & 318/2010006-04: Failure to Translate Design Calculation Setpoint of
Phase Overcurrent Relay on Feeder Breakers.
2.4
Breaker 2BKR152-2501 (4 kV Bus 25 Normal Feed) Failed to Trip Open
a.
InSpElction Scope
The team reviewed design requirements, drawings, and maintenance history of the
2BKR152-2501 breaker. The breaker inspection reviewed the maintenance practice and
procedure of overhauling the 4 kV breakers to determine if adequate test acceptance
criteria were established and followed vendor recommendations. The team reviewed
Constellation's root cause analysis report for the 2BKR152-2501 to determine the
adequacy of the evaluation and the appropriateness of the extent-of-condition review.
Independent reviews of the design documentation, drawings, maintenance history, and
field walkdowns were performed to validate the cause of the breaker failure.
Enclosure
21
Additionally, operations, maintenance, and engineering staff were interviewed to confirm
the c,bservations and causes cited in Constellation's evaluation of this issue. The team
reviewed the adequacy of associated preventive maintenance, corrective actions, and
post maintenance testing performed on the 2BKR152-2501 breaker. Bus 25 supplies
power to three Unit 2 circulating water pumps.
No findings of significance were identified for this equipment issue. The team
determined that this failure of 2BKR 152-2501 to open had no adverse consequence
during this event.
2.5
Breaker 2BKR252-2201 (13 kV Unit 2 RCP Buses Normal Feed) Failed to Trip Open
a.
Inspection Scope
The team reviewed design requirements, drawings, and maintenance history of the
2BKR252-2201 breaker. The team reviewed the maintenance practice and procedure of
overhauling the 13.8 kV breakers to determine if adequate test acceptance criteria were
established and followed vendor recommendations. Constellation concluded the cause
of the breaker failing to open was infant mortality (Le., manufacturing defect). The team
reviewed Constellation's root cause analysis report for the 2BKR252-2201 to determine
the adequacy of the evaluation and the appropriateness of the extent-of-condition
review. Independent reviews of the design documentation, drawings, maintenance
history, and field walkdowns were performed to validate the cause of the breaker failure.
Additionally, operations, maintenance, and engineering staff were interviewed to confirm
the observations and causes cited in Constellation's evaluation of this issue. The team
reviewed the adequacy of associated preventive maintenance, corrective actions, and
post maintenance testing performed on the 2BRK252-2201 breaker.
b.
Findings
No findings of significance were identified.
3.
Human Performance
3.1
Event Diagnosis and Crew Performance
a.
Inspection Scope
The team interviewed the operations crew that responded to the February 18, 2010,
event, including three senior reactor operators, the shift manager, the control room
supervisor, the shift technical advisor, two reactor operators, and three equipment
operators to determine whether the operators performed in accordance with procedures
and training. The team also reviewed narrative logs, post-transient reports, condition
reports, PPC trend data, and procedures implemented by the crew.
b.
Findings/Observations
Deficient Procedure Guidance for CVCS Letdown Restoration
Enclosure
22
rntroduction: A self-revealing Green NCV of TS 5.4.1.a, "Procedures," was identified
because Constellation did not establish adequate procedures for restoration of CVCS
letdown flow. Deficient operating instructions prevented timely restoration of letdown
flow following letdown isolation, which ultimately led to exceeding the TS high limit for
pressurizer level.
Description: On February 18, 2010, Unit 1 was operating at 93% reactor power in
preparation for main steam safety valve testing with the 11 and 13 charging pumps
operating and increased letdown flow balanced with cparging flow. At 8:24 a.m., a
phase to ground overcurrent fault on 12B RCP switchgear resulted in an automatic reactor trip on Unit 1. Protective relaying isolated plant service transformer P-13000-2,
which de-energized Unit 1 4 kV bus 14. Instrument Bus 1Y10, which is normally fed
from 4 kV Bus 14, de-energized, isolating CVCS letdown by closing letdown isolation
valvI31-CVC-515. The 1B EDG automatically started on bus undervoltage and re
powered 4 kV Bus 14 about 8 seconds later.
Charging pump 13 stopped on loss of power when 14 Bus de-energized and charging
pump 11, powered from 4 kV Bus 11, continued running. At 8:31 a.m., operators re
started charging pump 13. Charging pumps remained running and pressurizer level
incrE~ased as expected. Operators performed makeup to the CVCS Volume Control
Tank (VCT) from 8:50 a.m. to 9:11 a.m. in order to maintain VCT inventory while the two
running charging pumps transferred VCT contents into the pressurizer. At 8:58 a.m., 34
minutes after the reactor trip, and with pressurizer level approaching the high end of the
EOP pressurizer level control band (180"), operators turned off charging pump 13.
Charging pump 11 continued to run in anticipation of restoring letdown. At 9:02 a.m.,
operators stopped charging pump 11 because pressurizer level was above the EOP high
level limit.
At 9:12 a.m., operators made their first attempt to restore letdown in accordance with 01
2A, "Chemical and Volume Control System", Section 6.7, "Starting Charging and
Letdown" by re-starting charging pump 11 and shortly thereafter opening letdown
isolation valves. They were not successful in restoring letdown. Subsequent post-event
analysis of system parameter data stored on the plant computer indicated that excess
flow check valve 1-CVC-343 was closed. Inadequate procedural guidance prevented
operators from re-opening the check valve to establish letdown flow. The procedure for
starting letdown consisted of setting letdown downstream control valves at 20% open in
manual, starting a charging pump to cool the letdown stream, then opening letdown
upstream isolations 1-CVC-515 and 1-CVC-5i6 to establish letdown flow. 01-2A did not
contain any information related to the possibility that excess flow check valve 1-CVC-343
might be closed and did not provide direction for opening the valve.
Operators were confused by indicated letdown flow remaining downscale and took about
7 minutes re-confirming the system lineup and monitoring their instrumentation before
stopping charging pump 11. They did not use 01-2A, Section 6.6, "Securing Charging
and Letdown" to stop charging and letdown because letdown was not yet established.
Initial conditions for using Section 6.6 were not met. Operators did not recognize a need
for simultaneously stopping charging and letdown in accordance with the general
methodology of Section 6.6. An additional 17 minutes elapsed from the time operators
stopped the charging pump 11 until they closed the upstream letdown isolation valves.
Enclosure
I
j.
23
Post-event data analysis showed the downstream letdown* piping temperature steadily
incre:ased into the 400
0 to 500°F range during the 17 minutes between stopping the
chan~ing pump and closing the upstream letdown isolation valves because of hot reactor
coolant flowing in the letdown line through the 10 gallons per minute (gpm) orifice which
bypasses around the excess flow check valve. Typically, reactor coolant is cooled by
charging flow through the letdown regenerative heat exchanger to about 220°F in the
letdown line. It is postulated that during letdown restoration attempts, the ReS which
was greater than 2000 psi pressure, re-pressurized the letdown line which rapidly
collapsed steam voids in the hot (400°F-500°F) letdown piping and re-closed the excess
flow check valve because of water hammer. A differential pressure was then established
across the check valve, maintaining it closed. The restoration method provided by
procedure OI-2A did not contain actions necessary for pressure equalization across this
spring-loaded check valve.
During the second letdown restoration attempt at 10:44 a.m., letdown continued to flow
through the bypass orifice for 21 minutes after stopping charging pump 11. This action
again heated the letdown line to near reactor coolant temperature. On the third attempt
at 11 :39 a.m., operators closed letdown isolation valves just 2 minutes after stopping the
char!Jing pump, which left the letdown line in a relatively cool state, such that the
transient conditions on the fourth and final attempt did not re-close the excess flow check
valve. Operators made a total of four attempts to restore letdown over 5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> before
letdown was finally restored at 1 :17 p.m.
Pressurizer level remained above the specified limit in EOP-1 for all but a few minutes of
approximately 5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> following the reactor trip. Throughout this period, operators
attempted to control pressurizer level from the EOP high level limit of 180" to the normal
full power level of 215". This range was based on the constraints of contrOlling
pressurizer level below the TS high limit of 225" and high enough to prevent overfilling
the VCT. With letdown unavailable, operators were only able to lower pressurizer level
through the 6 gpm reactor coolant pump seal bleed off that returns to the VCT.
The team observed that unnecessarily conservative procedural requirements for
ensuring adequate shutdown margin in NEOP-301, "Operator Surveillance Procedure"
contributed to the operating crew's sense of urgency for letdown restoration. Operators
rec09nized that the 2400 gallon ReS boration required to satisfy the requirements of
NEOP-301 would cause pressurizer level to significantly exceed the TS high level limit if
performed with letdown isolated.
Other options existed for controlling VeT level such that bleed off could be allowed to
reduce pressurizer level to within the EOP band. These included intentionally draining
the VeT to the liquid waste system and aligning bleed off flow to return to the reactor
coolElnt drain tank instead of to the VeT. However, the station does not have an
abnormal operating procedure for responding to a sustained loss of letdown and
therefore no procedural guidance existed for using other methods to control veT level.
Around noon, shortly after the third attempt to restore letdown, operators became
involved in shifting main turbine gland sealing steam supply from main steam to auxiliary
steam and failed to control ReS temperature. Loop temperature rose approximately
5°F, causing pressurizer level, already high at 215", to rise and peak at 231."
Pressurizer level remained above the TS 3.4.9 high limit of 225" for apprOXimately 7
Enclosure
24
minutes until operator actions which were taken to lower RCS temperature succeeded in
reducing level to below the TS limit
The excess flow check valve did not re-close on the fourth restoration attempt. letdown
was successfu Ily re-established at 1317, approximately 5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> after event initiation.
COnl:;tellation has established procedure guidance relating to letdown restoration
following closure of the excess flow check valve. The issue was entered into their CAP
for further evaluation as CR 2010-001378.
Analysis: The performance deficiency is that Constellation did not establish adequate
procedures for restoring letdown. Multiple factors contributed to pressurizer level
exceeding the TS high limit. These included time pressure from overly conservative
procedure requirements related to maintaining shutdown margin, filling the pressurizer
above the EOP band when RCS temperature was below its nominal no*load value,
makeup to the VCT to the high end of its control band when pressurizer level was
already high, the absence of proceduralized options for controlling VCT level, and
inattentiveness to reactor coolant temperature control. However, inadequate procedure
guidance for letdown restoration is the primary reason which led to operation outside of
EOP pressurizer level limits for an extended period of time and unnecessarily challenged
operators in their attempts to maintain pressurizer level control.
The team determined this finding is more than minor because it is associated with the
procedure quality attribute of the Mitigating Systems Cornerstone and affected the
cornerstone objective to ensure the availability, reliability, and capability of systems that
respond to initiating events to prevent undesirable consequences (i.e., core damage).
The finding is of very low safety significance (Green) because it is not a design or
qualitfication defiCiency. did not represent a loss of a safety function of a system or a
single train greater than its TS allowed outage time, and did not screen as potentia!ly risk
significant due to external events. This finding has a crosscutting aspect in the area of
Human Performance, resources, because Constellation did not ensure that procedures
for restoring CVCS letdown were complete and accurate (H.2(c>>.
Enforcement: TS 5.4.1.a requires, in part, that written procedures be established,
implemented, and maintained for activities described in Appendix A of Regulatory Guide
(RG) 1.33, "Quality Assurance Program Requirements (Operation}." Specifically,
Section 3 of RG 1.33, Appendix A, "Instructions for energizing, filling, venting, draining,
startup, shutdown, and changing modes of operation should be prepared, as
appropriate, for the following systems," includes the Letdown/Purification System.
Contrary to the above, on February 18, 2010, the operators were unable to restore
charging and letdown using the existing instructions of OI-2A, "Chemical and Volume
Control System," due to inadequacy of the procedure. Because this issue is of very [ow
safety significance {Green) and Constellation entered this issue into their corrective
action program as CR 2010-001378, this finding is being treated as an NCV consistent
with Section VJ.A.1 of the NRC Enforcement Policy. (NCV 05000317/318/2010006-05,
Failed to Establish Adequate Procedures for Letdown Restoration).
3.2
Communications and Emergenqy Plan Applicability
a.
InsQ~:lction Scope
Enclosure
25
This event involved an automatic reactor trip of both units with multiple complicating
degraded equipment issues. Each unit lost one 500 kV offsite power supply (the Red
Bus). In addition, Unit 2 lost forced RCS circulation when all four RCPs tripped, the 28
EDG failed to reenergize the Unit 2 24 4 kVafety bus, and the Unit 2 normal heat
removal sink (main condenser) was unavailable for an extended time. Operators notified
the NRC of the event at 11 :47 a.m. on February 18 in accordance with 10 CFR 50.72.
Operators determined that emergency action level (EAL) entry criteria were not met and
accordingly did not declare an emergency event. The team reviewed operator logs,
emergency procedures, the Emergency Plan, plant operating data, and interviewed
station personnel to verify operators properly assessed the EAL entry criteria and
notified the NRC of the event.
b.
Findings
No findings of Significance were identified.
4.
Organizational Response
4.1
Immediate Response and Restart Readiness Assessment
a.
InSpE!ction Scope
The team interviewed personnel, reviewed various procedures and records, observed
plant operators and station meetings, and performed plant walkdowns to assess station
personnel's immediate response to the event and restart readiness assessment. The
licensee restart readiness assessment was performed in accordance with CNG-OP
1.01-1006, Post-Trip Reviews, Rev. 1.
No findings of Significance were identified.
Operators promptly announced the event, implemented the appropriate emergency
operating procedures, and correctly assessed EALs. However, human performance
deficiencies and/or procedure deficiencies led to Unit 1 exceeding the TS pressurizer
level limit (Section 3.1) and untimely verification of offsite power source availability.
Constellation augmented the on-shift staff promptly to support initial diagnosis and
corrective actions to address the numerous degraded equipment problems.
The post-trip review was sufficient to ensure operator performance issues and significant
equipment issues were identified and addressed. Notwithstanding, the team identified
several deficiencies which posed challenges to the effectiveness of the licensee restart
readiness assessment (CR 2010-004502). The team discussed each issue with licensee
management who entered the issues into the corrective action program, as applicable.
One notable issue was that station personnel did not quarantine several failed
components (breaker 152-2501, 2B EDG oil sensing line contents, relay 251 G/B-22-2).
This adversely limited the as-found information available to diagnose the failure
mechanisms.
4.2
Post-Event Root Cause Analysis and Actions
. Enclosure
26
a.
Inspection Scope
The team reviewed the RCAR for the 2010 Dual Unit Trip to determine whether the
causes of the event and associated human performance and equipment challenges
were properly identified. Additionally, the team assessed whether interim and planned
long term corrective actions were appropriate to address the cause(s).
No findings of significance were identified.
The RCAR properly evaluated causes and appropriate corrective actions for several
equipment challenges. For example, evaluation and corrective actions for the Unit 1 roof
leakage which initiated the ground fault event were comprehensive. In addition to the
root cause, the RCAR identified several contributing causes including deficient
maintenance rule implementation and performance monitoring, over reliance and
inadequate vendor oversight, incomplete incorporation of Quality Assurance findings,
and insufficient engineering involvement in roof construction. Interim corrective actions
were appropriate and long term actions were being developed through the corrective
action program.
In several other areas the team determined the RCAR lacked depth and technical rigor
in identifying and assessing potential causes. In each case the RCAR developed an
explanation for what may have caused the event or equipment response, but did not fully
develop other potential causes. Examples included:
RCAR did not identify the failure to implement an Agastat relay monitoring
program when the 10 year replacement PM was eliminated (2B EDG failure);
RCAR conclusion that loose diaphragm retaining ring screws on the Agastat relay
were caused by vibration and were the result of a manufacturing defect were not
well supported by the contracted failure analysis or data evaluation (2B EDG
failure);
Inforr:nation that the relay induction disc did not freely rotate back to the original
position during bench troubleshooting. was not incorporated into the RCAR (relay
2RY251G/B-22-2 failure);
RCAR did not thoroughly review previous internal OE regarding induction disc
failure on CO-8 type relays. Station personnel did not recognize the sensitivity of
the induction disc to sticking/binding (relay 251 G/B-22-2 failure);
RCAR did not include or address the 2008 as-found inspection results which
found the armature linkage misaligned and the trip coil loose. This was an
unexpected and infrequent occurrence (breaker 152-2501 failure); and
ReAR concluded the 152-2501 breaker failure was due to mechanical binding in
the trip linkage caused by human error during the October 2008 trip armature bolt
replacement. However, corrective actions did not investigate other breaker
maintenance performed by these technicians during that time period.
Enclosure
27
The team reviewed these issues and determined that none of these issues involved
violations of regulatory requirements or were already described as part of the previously
discussed violations in this report.
Enclosure
28
4.3.
Revi'9w of Operating Experience
a.
Inspection Scope
The team reviewed Constellation's use of pertinent industry and station operating
experience (OE), including evaluation of potential precursors to this event.
b.
Findings
No findings of significance were identified.
The team identified several instances where Constellation had not effectively evaluated
or initiated actions to address related station or industry operating experience issues.
Examples included:
- Unit 1 and Unit 2 45 foot switchgear room roof leakage onto electrical switchgear
had been identified numerous times since 2002, but not corrected. Fifty-eight
open work orders for roof leaks, several> 24 months old, had not been
implemented (Section 2.1).
- Industry OE has reported numerous problems with Agastat series 7000 relays;
several affecting reliability of the actuation setpoint. Yet engineers extended both
the service life and calibration periodicity of the EDG lube oil pressure trip time
delay relays beyond the vendor specified periods without adequate technical
basis (Section 2.2).
- Technicians routinely did not consider relay actuation outside of the acceptance
band to be a test failure. Often no condition report was initiated and no
drift/performance trending was performed. Corrective action was often limited to
adjusting the as-left setpoint to within the acceptance band (e.g, agastat 7000
series time delay relays, CO-8 overcurrent protection relays) (CR 2010-004090).
The team reviewed these issues and determined that none of these issues involved
violations of regulatory requirements or were already described as part of the previously
discussed violations in this report.
5.
Risk Significance of the Event
a.
Initial Assessment
The initial risk assessment for this event is documented in the enclosed SIT charter.
b.
Final Assessment
Onsite follow-up and discussions with the Constellation PRA staff verified that there
were no additional plant conditions or operator performance issues that significantly alter
the initial event risk assessments performed for both units. The Unit 1 reactor trip
estimated conditional core damage probability (CCDP) was calculated to be 2.6 E-6 for
the February 18, 2010 reactor trip. The Unit 2 reactor trip CCDP, accounting for a loss
of reactor coolant forced Circulation (all RCPs tripped), loss of heat sink (main
Enclosure
.1
29
condenser}, and failure of the 28 EDG to run, was estimated to be 1.5 E-5 for the
February 18, 2010 event
40A3 Follow~up of Events
(Closed) Licensee Event Report (LER) 05000317/2010-001, Reactor Trip Due to Water
Intrusion into SWitchgear Protective Circuitry
On February 18, at 8:24 a.m., the Unit 1 reactor automatically tripped from 93 percent
reactor power in response to a RCS low flow condition. Water had leaked through the
auxiliary building roof into the 45' switchgear room, causing an electrical ground which
tripped the 128 RCP, thereby initiating the reactor protection system trip on RCS low
flow. Three of the four Unit 1 Reps continued operating. The electrical ground and
failure of a ground fault protection relay caused service transformer P-13000-2 to isolate,
thereby deenergizing the 144 kV safety bus and the 1Y1 a 120 volt instrument bus. The
1B EDG automatically started and reenergized the 14 bus as designed. The LER
accurately described operator response to the event. The team reviewed the LER and
idenlified no findings of significance beyond those previously documented in this report
(NRC Inspection Report No. 05000317/2010006). This LER stated a supplemental LER
will document a complete description of corrective actions after the event analysis and
cause determination is complete. This LER is closed .
. 2
(Cloe;ed) Licensee Event Report (LER) 05000318/2010-001, Reactor Trip Due to Partial
On February 18, at 8:24 a.m., the Unit 2 reactor automatically tripped from 99.5 percent
reactor power due to a loss of power to all four Reps and the associated reactor
proteiCtion system RCS low flow trip. The event emanated from a ground fault on Unit 1
(see Section 2.1). A ground OIC relay failed to actuate as designed, permitting the Unit
1 ground OIC condition to reach Unit 2. Unit 2 electrical protection responded by
deenergizing the 500 kV"Red Bus" offsite power supply and multiple onsite electrical
buses including the 24 4 kV safety bus. The 28 EDG started as designed, but tripped on
low lube oil pressure (see Section 2.2). The LER accurately described operator
response to the event. The team reviewed the LER and identified no findings of
significance beyond those previously documented in this report (NRC Inspection Report
No.05000317/2010006}. This LER stated a supplemental LER will document a
complete description of corrective actions after the event analysis and cause
determination is complete. This LER is closed.
40A6 Meetings, Including Exit
Exit Meeting Summary
On April 30, 2010, the team presented their overall findings to members of Constellation
management led by Mr. G. Gellrich, Site Vice President, and other members of his staff
who l:lcknowledged the findings. The'team confirmed that proprietary information
reviewed during the inspection period was returned to Constellation.
Enclosure
Licensee Personnel
G. Gellrich
K. Allor
P. Amos
P. Darby
S. Dean
M. Draxton
D. Fitz
M. Flynn
D. Frye
M. Gahan
G. Gellrock
S. Henry
J. Koebel
D. Lauver
W. Mahaffee
J. McCullum
K. Mills
P. O'Malley
T. Riti
K. Roberson
A. Simpson
R. Stark
T. Trepanier
Others
S. Gray
M. Griffin
1-1
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Site Vice President
Senior Operations Instructor
Performance Improvement
Principal Assessor, Engineering Quality Performance Assessment
Manager, Maintenance
Manager, Nuclear Training
Communications
HR Director
Manager. Operations
GS, Design Engineering
Supervisor
Manager, Work Management
Director, Licensing
Supervisor, Chemistry Operation
Supervisor, Instrumentation and Controls
Assistant Operations Manager
Quality Performance Assessment
GS, System Engineering
Manager, NSS
Engineering/Licensing
Design Engineering
Plant General Manager
Power Plant Research Program Manager, Department of Natural
Resources, State of Maryland
Nuclear Emergency Preparedness Coordinator, Department of the
Environment, State of Maryland
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened
05000317/318f2010006-01
05000317/318f2010006-02
05000317/318/2010006-03
Failure to Thoroughly Evaluate and Promptly
Correct Degraded Conditions Associated with
Auxiliary Building Roof Leakage {Section 2.1}
Inadequate Preventive Maintenance Results in the
Failure of the 2B Emergency Diesel Generator
(Section 2.2)
Failure to Evaluate Degraded Conditions
Associated with CO-8 Relays and Implement
Attachment 1
1-2
Timely and Effective Action to Correct the Condition
05000317/318/201 0006-04
05000317/3'18/20 1 0006-05
Opened and Closed
05000317/201 0-001
Drawings
Adverse to Quality (Section 2.3)
Failure to Translate Design Calculation Setpoint of
Phase Overcurrent Relay on Feeder Breakers
(Section 2.3)
Faifed to Establish Adequate Procedures for
Letdown Restoration (Section 3.1)
LER
Reactor Trip Due to Water Intrusion into Switchgear
Protective Circuitry (Section 40A3.1)
LER
Reactor Trip Due to Partial Loss of Offsite Power
(Section 40A3.2)
LIST OF DOCUMENTS REVIEWED
61004, Single Line Meter & Relay Diagram 13 kV System, Rev. 26
61001SH0001, Electrical Main Single Line Diagram FSAR Fig. No. 8-1, Rev. 42
63070SH0009, Schematic Diagram 13 KV Service Bus 22 RCP Bus Feeder Breaker 252-2201,
Rev. 11
63049, AC Schematic Diagram Service Bus 22 & Service Transformer P-13000-2, Rev. 17
Condition Reiports (CR)
IRE-000-433
CR 2009-008115
CR 2010-001707
2010-001779
2010-001780
2010-001781
2010-001782
2010-001783
2010-001784
2010-001787
2010-001813
2010-001888
2010-002875
2010-004411
2010-004493
2010-004502
2010-004613
2010-004652
2010-004672
2010-004673
2010-004674
2010-001699
2010-001700
IRE-004-399
CR 2009-008537
CR
IRE-004-400
CR 2009-008635
CR
IRE-011-621
CR 2010-001330
CR
IRE-011-769
CR 2010-001340
CR
I RE-020-768
CR 2010-001351
CR
I RE-020-769
CR 2010-001355
CR
IRE-020-776
CR 2010-001381
CR
IRE-022-227
CR 2010-001516
CR
IRE-026-951
CR 2010-001517
CR
IRE-D28-751
CR 201 0-001544
CR
IRE-031-691
CR 2010-001553
CR
IRE-032-766
CR 2010-001586
CR
CR 2008-001582
CR 201 0-001592
CR
CR 2008-002458
CR 201 0-001682
CR
CR 2009-004060
CR 201 0-001685
CR
CR 2009-004074
CR 2010-001690
CR
CR 2009-004606
CR 2010-001691
CR
CR 2009-005508
CR 2010-001671
CR
CR 2009-00:5629
CR
CR 2009-006187
CR
Attachment 1
1-3
Maintenance Orders
MO #1200801597, Replace Flex Hoses on the 18 EDG
MO #2199901416, Calibrate 2B EDG Lube Oil Pressure Gauge, 2-PI-4796
MO #2200000476, Perform E-19 on 2B EDG Agastat Relays
MO #2200201832, 2B EDG Engine Stop Relay
MO #2200401152, 2B EDG Engine Stop Relay
MO #2200501401, 2B EDG Engine Stop Relay
MO #2200700554, Replace Flex Hoses on the 2A EDG
MO #2200700555, Replace Flex Hoses on the 2B EDG
MO #2200700852, 2B EDG Engine Stop Relay
Operability Evaluation
OE-2009-003712
Procedures
Auxiliary Building Walkdown Results, MN-1-319 "Structure and System Walkdowns," Rev. 5
Auxiliary Building Walkdown Results, MN-1-319 "Structure and System WaIkdowns, "Rev. 7
1 0-02 uRain/Snow Water Intrusion Compensatory Measures,>> Rev. 1
CNG-AM-1.01-2000, "Scoping and Identification of Critical Components," Rev. 00200
CNG-CA-1.01-1000, "Corrective Action Program," Rev. 0200
CNG-OP-1.01-1006, "Post Trip Reviews," Rev. 00001
CNG-OP-1.01-2000, "Operations Logkeeping and Station Rounds," Rev. 00100
CNG-QL-1.01-1007, "Quality Performance Assessment Process," Rev. 00201
CNG-PR-1.01-1009, "Procedure Use and Adherence Requirements," Rev. 00400
FTE-87, "Powell 13.8 kVType PVDH Vacuum Circuit Breaker Inspection," Rev. 00101
FTE-51A, "General Electric Cubicle Inspection," Rev. 2
FTE-59, "Periodic Maintenance, Calibration and Functional Testing of Protective Relays," Rev. 5
MN-1-319 "Structure and System Walkdowns," Rev. 7
NO-1-200, "Control of Shift Activities, Rev. 04401
NO-1-201, "Calvert Cliffs Operating Manual," Rev. 02000
OI-2A, "Chemical and Volume Control System," Rev. 55/Unit 1
Miscellaneous
Control Room Operations NarratiVe Logs
Operations Administrative Policy 90-7, Guidelines, System Expert and Shift Crew Ownership
Program Guidelines and Expectations, January 27,2010, Change 15
Plant Areas System 102 Walkdowns, 1- Unit 1 performed January 5.2010, & March 31, 2010
System 102 "Plant Areas," Maintenance Rule Scoping Document, Rev. 30
Site Roof Leakage Condition Report Scoping Document
U-1 Alarm History Printout for February 18, 2010
U-2 Alarm History Printout for February 18, 2010
U-1 Sequence of Events Recorder Printout for February 18,2010
U-2 Sequence of Events Recorder Printout for February 18, 2010
Engineering Service Package ES200100067, Revision 1, Delete Requirement in E-406
Sec 234.0.1 to Change Out Agastat Prior to Ten Years and Remove Testing
Recommendations to VTM 15-167-001
Procedure E-406, Rev. 0, Installation and Replacement for Agastat Relays
R001617, Revision 4, Guideline for Testing Agastat Relay Models
Constellation Nuclear Generation Fleet Administrative Procedure CNG-CA-1.01-1 004
Root Cause Analysis, Revision 00301
Attachment 1
1-4
Procedure FTI-328, Revision 1, Calibration Check/Calibration of Allen-Bradley Pressure
Switches
Rover Maintenance Approval and Closeout Form, MN-1-101, Revision 03601, 2A EDG
Oil Sensing Line Flush
Calvert Cliffs SUrveillance Test Procedure, STP 0-8B-2, Revision 26, Test of 2B DG and
4 kV Bus 24 LOCI Sequencer
Calvert Cliffs Surveillance Test Procedure, STP 0-8A-2, Revision 26, Test of 2A DG and
4 kV Bus 24 LOCI Sequencer
Operating Experience OE13852 - Inadequate Venting of the Emergency Diesel
Generator Lubricating Oil System
Sch(:)matic Diagram Diesel Generator 1\\10. 2B Engine Control, No. 63086SH0010,
Revision 39
Work Order C90791765, 2B Diesel Generator Failed to Start and Load on the 24 4 kV
Operating Experience, ACE 013617, Surry EDG Agastat Relay Failure
Constellation Nuclear Generation Fleet Administrative Procedure CNG-AM-1.01-1 018
Preventive Maintenance Program, Revision 00400
Vendor Manual 15167-001-1001, Agastat Timing Relays 7000 Series
Vendor Manual 15167-001-1005, Tyco Electronics
Herguth Labratories Crankcase Oil Sample Data
Troubleshooting Data Sheet to Determine Cause of 2B EDG Trip after Closing onto 24 4
kVBus
CCNPP Procurement Engineering Specification, PES - 25180. Revision 17, Agastat
Relays and Associated Hardware
Maintenance Strategy 2RY2DG2BAlT3A Relay
2-PS-4798 Master Calibration Data Package, 2/19/10
Root Cause Analysis
CNG-CA-1.01-1004 "Root Cause Analysis" Dual Unit Trip, Rev 00301
Apparent C~luse Evaluation
IRE-007-70S
Calculations/Engineering Evaluation Reports
E-90-058, Blreaker 252-1101, 1102, 1103, Rev. 2
E-90-061, Breaker 252-2101, 2102, 2103, Rev. 2
E-90-062, BI'eaker 252-2201, Rev. 2
RCS Letdown Line Evaluation for Potential Water Hammer dated 3/16/10
Completed Tests/Surveillances
E-30, 4.16 kV Magne-Blast Circuit Breaker Overhaul Procedure, Performed 10/04/04
FTE-51 , 4 kV General Electric Magne-Blast Circuit Breaker Inspection, Performed 11/18/08,
4114105
FTE-59. Periodic Maintenance, Calibration and Functional Testing of Protective Relays,
Performed 04/06/00,03126/03,05/03/04, 10/01/05,05/08/07, 10/10/07,03/08/08,
11120108, 02128109
FTE-87, Powell 13.8 kV Type PVDH Vacuum Circuit Breaker Inspection, Performed 3/15/07
STP-O-90-1 and STP-0-90-2, TrAC Sources and Onsite Power Distribution Systems 7 Day
Operability Verification, Rev. 22
Attachment 1
1-5
LlCDF
CFR
CR
eves
ESDP
gpm
IMC
kV
LlLERF
LER
NRC
OC
RCAR
SPM-A
TD
TS
LIST OF ACRONYMS
Apparent Violation
Calvert Cliffs
Increase in Core Damage Frequency
Code of Federal Regulations
Condition Report
Chemical and Volume Control System
Division of Reactor Projects
Division of Reactor Safety
Emergency Action Level
Emergency Operating Procedure
Emergency Shutdown Panel
Gallons per Minute
Inspection Manual Chapter
Kilovolt
Increase in Large Early Release Frequency
Licensee Event Report
Non-cited Violation
Nuclear Regulatory Commission
Operating Experience
Preventive Maintenance
Plant Onsite Review Committee
Plant Process Computer
Root Cause Analyses Report
Reactor Coolant Pump
Regulatory Guide
Significance Determination Process
Shift Manager
Woodward SPM-A Synchronizer
Senior Reactor Analyst
Special Inspection Team
Standardized Plant Analysis Risk
Surveillance Test
Time Delay
Technical Specification
Under-Voltage
Volume Control Tank
Attachment 1
2-1
UNITED STATES
NUCLEAR REGULATORY COMMISSION
REGION I
475 ALLENDALE ROAD
KING OF PRUSSIA, PA 19406-1415
SPECIAL INSPECTION TEAM CHARTER
February 22,2010
MEMORANDUM TO:
Glenn Dentel, Manager
Special Inspection Team
David Kern. Leader
Special Inspection Team
FROM:
David C. Lew, Director
IRA!
Division of Reactor Projects
Darrell J. Roberts, Director
IRA!
Division of Reactor Safety
SUBJECT:
SPECIAL INSPECTION TEAM CHARTER
CALVERT CLIFFS PARTIAL LOSS OF OFFSITE POWER AND
DUAL UNIT TRIP WITH COMPLICATIONS ON
FEBRUARY 18, 2010
In accordance with Inspection Manual Chapter (IMC) 0309, "Reactive Inspection Decision
Basis for Reactors," a Special Inspection Team (SIT) is being chartered to evaluate a Calvert
Cliffs dual unit trip with complications which occurred on February 18,2010. The decision to
conduct this special inspection was based on meeting multiple deterministic criteria (multiple
failures in equipment needed to mitigate an actual plant event, significant unexpected system
interactions, and events involving safety related equipment deficiencies) specified in Enclosure
1 of IMC 0309 and the event representing a preliminary conditional core damage probability in
the low E-6 range for Unit 1 and low E-5 range for Unit 2.
The SIT will E:lxpand on the inspection activities started by the resident team immediately after
the event. The team will review Constellation's organizational and operator response to the
event, equipment and design deficiencies, and the causes for the event and subsequent issues.
The team will collect data, as necessary, to refine the existing risk analysis. The team will also
assess whether the SIT should be upgraded to an Augmented Inspection team.
The inspection will be conducted in accordance with the guidance contained in NRC Inspection
Attachment 2
G. Dentel, D. Kern
2-2
Procedure 93812, "Special Inspection," and the inspection report will be issued within 45 days
following the, final exit meeting for the inspection.
The special inspection will commence on February 22,2010. The following personnel have
been assigned to this effort:
Manager:
Glenn Dentel, Branch Chief,
Projects Branch 1, Division of Reactor Projects (DRP). Region I
Team Leader:
David Kern, Senior Resident Inspector
DRP, Region I
Full Time Members:
Peter Presby. Operations Inspector
Division of Reactor Safety (DRS). Region I
Manan Patel, Electrical Inspector
DRS, Region I
Brian Smith, Resident Inspector
DRP, Region I
Part Time Member:
William Cook, Senior Reactor Analyst
DRS, Region I
Enclosure: Special Inspection Charter
Attachment 2
G. Dentel, D. Kern
2-3
The special inspection will commence on February 22, 2010.
been assigned to this effort:
The following personnel have
Manager:
Glenn Dentel, Branch Chief,
Projects Branch 1. Division of Reactor Projects (DRP). Region 1
Team Leader:
David Kern, Senior Resident Inspector
DRP, Region [
Full Time Members:
Peter Presby, Operations Inspector
Division of Reactor Safety (DRS), Region I
Manan Patel, Electrical Inspector
DRS, Region I
Brian Smith, Resident Inspector
DRP, Region I
Part Time Member:
William Cook, Senior Reactor Analyst
DRS, Region I
Enclosure: Special Inspection Charter
ccw/encl:
B. Borchardt, EDO (RidsEDOMailCenter)
B. Mallett, DEDO (RidsEDOMaHCenter)
E. Leeds, NRR
B. Boger, NRR
J. Wiggins, NSIR
S. CoHins, RA (R10RAMAIL RESOURCE)
M. Dapas, ORA (R1 ORAMAIL RESOURCE)
D. Lew, DRP (1~10RPMAIL RESOURCE)
J. Clifford, DR? (R1DRPMAIL RESOURCE)
D. Roberts, DRS(R1DRSMail Resource)
P. Wilson, DRS (R1DRSMaii Resource)
L. Trocine, RI OEDO
G. Dentel, DR?
N. Perry, DRP
J. Hawkins, DRP
S. Sloan, DRP
M. Davis, DRP, RI
C. Newgent, DRP, Resident OA
RidsNrrPMCalvertCliffs Resource
RidsNrrDorlLpl1-1 Resource
D. Screnci, PAO
N. Sheehan, PAO
R. Barkley, ORA
N. McNamara, SLO
D. Tifft, SLO
I
!
!
SUNSI Review Complete:
NP
(Reviewer's Initials)
Non-Public Designation Category: MD 3.4 Non-Public
B.1
(A.3 - A.7 or B.1)
DOCUMENT NAME: G:\\ORP\\BRANCH1\\CC-SIT CHARTER Final.doc
ML - will be obtained when ADAMS is available
After declaring this document "An Official Agency Record"'t will not be released to tI:le Public.
OFFICE
NAME
DATE
To receive a copy of this document, indicate in the box: ~c* =Copy without attachment/enclosure "E" =Copy with
h
fJ
"N" N
attac men enclosure
= o COP'
RIIDRP
I
RI/DRP
I
RI/DRS
I
RIIDRP
I
NPerry/NP
DKern/NP via
GDentel/GTD
DLew/JWC for
teleconf
02/22/10
02/22110
02122/10
02/22/10
RI/DRS I
DRoberts/PW
for
02/22/10
OFFICIAL RECORD COpy
Attachment 2
2-4
Special Inspection Team Charter
Calvert Cliffs Nuclear Power Plant
Dual Unit Trip with Complications due to a Partial Loss of Offsite Power
on February 18. 2010
. Backgrounl~:
At 8:24 a.m. on February 18, 2010, Calvert CUffs Unit 1 experienced an unexpected loss of the
12B reactor coolant pump (RCP). The loss of the RCP trip resulted in a valid reactor protection
system (RPS) actuation on low reactor coolant system flow and a Unit 1 trip.
At approximately the same time, Unit 2 experienced a loss of the 500 kV to 13.8 kV transformer
for the "Red Bus" (500 kV). The Red Bus is the feeder for offsite power for the Unit 1 "14" and
Unit 2 "24" 4 kV safety buses. Unit 2 experienced the following system/component responses
based on the loss of the Red Bus: loss of the non-safety related buses, a loss of load RPS trip
signal, a loss of all RCPs, and a Unit 2 trip. The loss of the non-safety related buses resulted in
the loss of the circulating water pumps, the main feedwater pumps, and condensate pumps, and
the subsequent loss of the normal heat sink. Bus 21 , the other Unit 2 safety 4 kV bus, normally
aligned to the Black Bus, remained energized.
The los$ of power to the "'14" and "24" 4 kV safety buses resulted in a valid start signal for the
1B and 28 EDGs, respectively. The 1B EDG started and re-powered the "14" safety bus;
however, thE! 2B EDG tripped during loading resulting in the loss of the "24" safety bus. This
resulted in the unavailability of the "B" safety train. Calvert Cliffs subsequently restored power
to the "24" safety bus via the Black Bus alternate power supply.
Unit 1 was c()oled down and entered a refueling outage that was originally scheduled to begin
on February 20,2010. Unit 2 was stabilized on natural circulation, and normal decay heat
removal was subsequently restored; the plant has entered a forced outage.
At the time of the event, the resident team responded to the control room and monitored
licensee actions to stabilize the plant and restore offsite power. An NRC regional inspector was
also deployed to the site to supplement the resident staff.
Basis for the Formation of the SIT:
The IMC 0309 review concluded that three deterministic criteria were met. The deterministic
criteria met included: 1) multiple failures of plant equipment in systems used to mitigate an
event; 2) Significant unexpected system interactions; and 3) events involving safety related
equipment deficiencies. These criteria were met based on the partial loss of offsite power due
to the transformer loss, and the subsequent failure of the 28 EDG to start and restore a safety
bus. In addition, the system interactions between the 12B RCP trip and the transient, which
resulted in the opposite 500 kV transformer loss, were unexpected. The Unit 2 transformer loss
also resulted in a complete loss of forced flow to Unit 2 due to the expected loss of all four
Reps, and the loss of the Unit 2 main condenser as a heat sin.k.
The event was also evaluated for risk significance because the IMC 0309 review concluded that
at least one deterministic criteria was met. Based upon best available information, the Region I
Senior Risk Analyst (SRA) conducted a preliminary risk estimate for each unit on February 18.
Using the Gn:lphical Evaluation Module initiating event quantification tool and the Calvert Cliffs
Unit 1 and Unit 2 Standardized Plant Analysis Risk (SPAR) models, the conditional core
Attachment 2
2-5
damage probability (CCDP) for Unit 1 was estimated to be in the low E-6 range, and the Unit 2
estimated CCDP was in the low E-5 range. On February 19, 2010, the SRA discussed these
results with the Constellation PRA staff and determined that the risk estimates (CCDP)
performed by Constellation favorably compared to the NRC SPAR model generated values.
Based upon the preliminary CCDP estimates, and in accordance with IMC 0309, the Unit 1 and
Unit 2 events fall within the overlap ranges of No Additional Inspection and Special Inspection
Team (SIT) for Unit 1, and SIT and Augmented Inspection Team (AIT) for Unit 2. After
consultation with NRC headquarters personnel, an SIT was initiated.
Objectives <of the Special Inspection:
The SIT will review Constellation's organizational and operator response to the event,
equipment and design deficiencies, and the causes for the event and subsequent issues. The
team will collect data, as necessary, to refine the existing risk analysis. The team will also
assess whether the SIT should be upgraded to an Augmented Inspection Team. Additionally,
the team leader will review lessons learned identified during this special inspection and, if
appropriate, prepare a feedback form on recommendations for revising the Reactor Oversight
Process (ROP) baseline inspection procedures.
To accomplish these objectives, the team will:
1. Develop a complete sequence of events including follow-up actions taken by
Constellation.
2. Review and assess the equipment response to the event. This assessment should
include an evaluation of the consistency of the equipment response with the plant's
d,esign and regulatory requirements. In addition, review and assess the adequacy of
any operability assessments, corrective and preventive maintenance, and post
maintenance testing.
3. Review and assess operator performance including procedures, logs,
communications (internal and external), and emergency plan implementation.
4. Review and assess the effectiveness of Constellation's response to this event. This
includes overall organizational response, failure modes and effect analysis
dl~veloped for the equipment challenges, causal analyses conducted, and interim
and proposed longer term corrective actions taken.
5. Evaluate Constellation's application of pertinent industry operating experience and
evaluation of potential precursors, including the effectiveness of any actions taken in
response to the operating experience or precursors; and
6. Collect any data necessary to refine the existing risk analysis and document the final
risk analysis in the SIT report.
Attachment 2
2-6
Guidance:
Inspection Procedure 93812, "Special Inspection", provides additional guidance to be used by
the Special Inspection Team. Team duties will be as described in Inspection Procedure 93812.
The inspection should emphasize fact-finding in its review of the circumstances surrounding the
event. It is not the responsibility of the team to examine the regulatory process. Safety
concerns identified that are not directly related to the event should be reported to the Region I
office for appropriate action.
The team will conduct an entrance meeting and begin the inspection on February 22, 2010.
While on site, the team Leader will provide daily briefings to Region I management, who will
coordinate with the Office of Nuclear Reactor Regulation, to ensure that all other parties are
kept informed. A report documenting the results of the inspection will be issued within 45 days
following the final exit meeting for the inspection.
This Charter may be modified should the team develop significant new information that warrants
review.
Attachment 2
3-1
DETAILED SEQUENCE OF EVENTS
February 18, 2010 Dual Unit Trip with Complications
The sequence of events was constructed by the team from review of Control Room Narrative
Logs, correc:tive action program condition reports, post transient review report, process plant
computer (FPC) data (alarm message file and plant parameter graphs) and plant personnel
interviews. The sequence of events is listed separately by Unit 1 and Unit 2.
UNIT 1 EVENT '"IMELINE
Clock Time IEvent Time
Description
0211812010
A phase to ground fault occurs on the 13 kV supply line to Unit 1
Reactor Coolant Pump (RCP) 12B Motor, upstream of 12B RCP
08:24:25:225 0.000 sec Breaker 252-14P02, which is already open (normal lineup).
Rep 12B Breaker 252-14P01 trips open on differential overcurrent
08:24:25:225 0.000 sec relay actuation, stopping 12B RCP.
Feeder Breaker 252-2104 to 13 kV Service Bus 21 trjps open, de-
energizing Unit 2 Non-vital balance of plant, Unit 2 Vital 4 kV Bus 24
08:24:27 :251 2.026 sec
and Unit 1 Vital 4 kV Bus 14.
208/120 VlAC Bus 12 de-energizes, resulting in isolation of the Unit
1 RCS letdown f10wpath in the Chemical and Volume Control
08:24:27:421 2.196 sec
System (CVCS).
13 kV Service Bus 22 Supply Breaker 252-2202 to Unir1 RCPs trips
open. Unit 1 RCPs are not affected as they are aligned to their
normal power supply from 13 kV Station Service Transformer P
08:24:28:803 3.578 sec
13000-1 through 13 kV Service Bus 12.
08:24:28:781 3.556 sec 500 kV Switchyard Red Bus Isolation Breaker 552-41 trips open.
500 kV SWitchyard Red Bus Isolation Breakers 552-21 and 552-61
trip open, completing the high side isolation 13 kV Station Service
08:24:28:783 3.558 sec
ransformer P-13000-2.
init 1 automatic reactor trip on reactor coolant low flow signal from
3% initial reactor power level. 3 of 4 Unit 1 reactor coolant pumps
08:24:29:110 3.885 sec
are still operating.
08:24:29:146 3.921 sec
Unit 1 reactor trip breakers open.
08:24:29:417 4.192 sec
Unit 1 turbine trip.
Undervoltage signal actuates on Unit 1 4 kV Vital Bus 14, initiating
08:24:29:423 4.198 sec the 1 B Emergency Diesel Generator start sequence.
Unit 14 kVVital Bus 14 Normal Feeder Breaker 152-1414 trips
.08:24:29:948 4.723 sec
open.
13 kV Service Bus 21 Supply Breaker 252-2103 to Transformer U
08:24:33:818 18.593 sec
4000-22 opens.
13 kV Service Bus 21 Supply Breaker 252-2102 to Transformer U
08:24:33:818 8.593 sec
4000-21 opens.
13 kV Service Bus 21 Supply Breaker 252-2101 to Transformer U
08:24:33:819 8.594 sec
4000-23 opens.
08:24:36:101 10.876 sec Emergency Diesel Generator 1 Breaches 810 rpm.
Emergency Diesel Generator 1 B Output Breaker 152-1403 to 4 kV
08:24:37:255 12.030 sec Vital Bus 14 closes.
IShutdown Sequencer on 4 kV Vital Bus 14 actuates, to re-start bus
08:24:37:26712.042 sec Iloads.
Attachment 3
3-2
UNIT 1 EVENT TIMELINE
Clock Time
Event Time
Description
08:24:37:748 12.523 sec 208/120 V/AC Bus 12 re-energizes.
08:24:37:774 12.549 sec Undervoltage signal clears on Unit 1 4 kV Vital Bus 14.
Reactor Operator backs up the automatic reactor trip signal by
08:24:42:015 16.790 sec depressing manual reactor trip pushbuttons.
08:24:55
30 sec
Crew enters EOP-O, Post-Trip Immediate Actions
Component Cooling Pump 11 is manually started. Component
08:26:35
2.17 min
Cooling system pressure and flow are restored.
08:31
7min
Charging Pump 13 re-started.
08:40
16 min
Crew exits EOP-O and enters EOP-1, Reactor Trip.
09:00
36 min
Pressurizer level out of EOP control band high, >180 inches.
09:02
38 min
Charging Pump 11 stopped.
Operators attempt to restore CVCS letdown (1 st attempt). Charging
09:12
48 min
Pum p 11 started. Letdown Isolations CVC-515 and 516 opened.
09:20
56 min
Charging Pump 11 sto~ed.
09:37
73 min
Letdown Isolation Valves CVC-515 and 516 closed.
10:41
2.28 hrs
Pressurizer level returns within EOP control band, <180 inches.
Operators attempt to restore CVCS letdown (2nd attempt).
Charging Pump 11 started. Letdown Isolations CVC-515 and 516
10:44
2.33 hrs
opened.
10:47
2.38 hrs
Pressurizer level out of EOP control band high, >180 inches.
11:07
2.72 hrs
Charging Pum p 11 stopped.
11:28
3.07 hrs
Letdown Isolation Valves CVC-515 and 516 closed.
Operators attempt to restore CVCS letdown (3rd attempt). Charging
11:39
3.25 hrs
Pump 11 started. Letdown Isolations CVC-515 and 516 opened.
11:47
3.38 hrs
Completed 4 hr report to NRC, as required per 10CFR50.72.
11 :50
3.43 hrs
Charging Pump 11 stopped.
11:52
3.47 hrs
Letdown Isolation Valves CVC-515 and 516 closed.
12:02
3.63 hrs
Pressurizer level above Tech Spec limit, >225 inches.
12:07
3.72 hrs
Pressurizer level returns within Tech Spec limit, <225 inches.
Completed STP-O-90-1, AC Sources and Onsite Power Distribution
12:07
3.72 hrs
Systems 7 Day Operability Verification.
12:11
3.78 hrs
Disconnects for 500 kV Switchyard Breaker 552-21 are opened.
12:14
3.83 hrs
Disconnects for 500 kV Switchyard Breaker 552-61 are opened.
12:15
3.85 hrs
Disconnects for 500 kV Switchyard Breaker 552-23 are opened.
12:17
3.88 hrs
Disconnects for 500 kV Switchyard Breaker 552-22 are opened.
12:18
3.90 hrs
Disconnects for 500 kV Switchyard Breaker 552-63 are opened.
13:06
4.70 hrs
Pressurizer level returns within EOP control band, <180 inches.
Operators attempt to restore CVCS letdown (4th attempt). Charging
Pump 11 started. Commenced ReS boration from 11 Boric Acid
13:09
4.75 hrs
Tank.
13:11
4.77 hrs
Pressurizer level out of EOP control band high, >180 inches.
Letdown Isolations CVC-515 and 516 opened. CVCS letdown
restored. Letdown Excess Flow Check Valve 1-CVC-343-CV
13:17
4.88 hrs
opened on 4th letdown restoration attempt.
13:30
5.10 hrs
Pressurizer level returns within EOP control band, <180 inches.
Attachment 3
3-3
UNIT 1 EVENT TIMELINE
Clock Time
Event Time
Description
Crew exits EOP-1 and enters OP-5, Plant Shutdown From Hot
13:38
5.23 hrs
Standby to Cold Shutdown.
13:46
5.37 hrs
Boratlon stopped, charging suction from VCT to lower VCT level.
13:58
5.57 hrs
Boration re-commenced from 11 Boric Acid Tank.
14:07
5.72 hrs
4 kV Vital Bus 14 Alternate Feeder Breaker 152-1401 closed.
Emergency Diesel Generator 1B Output Breaker 152-1403 to 4 kV
14:13
5.82 hrs
Vital Bus 14 opened.
14:15
5.85 hrs
Emergency Diesel Generator 1 B shutdown.
Boratlon completed. Approximately 2420 gaHons of boric acid
- 14:16
5.87 hrs
injected.
14:37
6.22 hrs
RCS sampled for boron. Concentration at 529 ppm.
16:00
7.6 hrs
RCS sampled for boron. Concentration at 622 ppm.
21:50
13.4 hrs
ts for 500 kV Switchyard Breaker 552-22 closed.
22:00
13.6 hrs
500 kV Switch yard Breaker 552-22 closed.
22:01
13.6 hrs
Disconnects for 500 kV SWitchyard Breaker 552-23 closed.
22:07
13.7 hrs
500 kV Switchyard Breaker 552-23 Closed.
02119/2010
12:01
27.6 hrs
SMECO now credited to 4 kV Bus 24.
02120/2010
17:05
Started 12B RCP.
19:20
~ Commenced RCS cooldown to MODE 5 per OP-5.
02121/2010
05:38
69 hrs
Unit 1 in MODE 5, RCS temperature < 200°F.
05:50
69.5 hrs
Divorced from SMECO, re-energized 500 kV Red Bus.
UNIT 2 EVENT TIMELINE
Clock Time
Event Time
Description
02118/2010
A phase to ground fault occurs on the 13 kV supply line to Unit 1
Reactor Coolant Pump (RCP) 12B Motor, upstream of 12B RCP
08:24:25:225 0.000 sec Breaker 252-14P02, which is already open (normal lineup}.
RCP 12B Breaker 252-14P01 trips open on differential overcurrent
08:24:25:225 0.000 sec relay actuation, stopping 12B RCP.
Feeder Breaker 252-2104 to 13 kV Service Bus 21 trips open, de-
energizing Unit 2 Non-vital balance of plant, Unit 2 Vital 4 kV Bus 24
i08:24:27:251 2.026 sec
and Unit 1 Vital 4 kV Bus 14.
208/120 VJAC Bus 22 de-energizes, resulting in isolation of the Unit
2 RCS letdown flowpath in the Chemical and Volume Control
08:24:27:478 2.253 sec
System (CVCS).
13 kV Service Bus 22 Supply Breaker 252-2202 to Unit 1 Reps trips
open. Unit 1 RCPs are not affected as they are aligned to their
normal power supply from 13 kV Station SerVice Transformer P
08:24;28:803 13.578 sec
13000-1 through 13 kV Service Bus 12.
108:24;28:781 :13.556 sec 500 kV Switchyard Red Bus Isolation Breaker 552-41 trips open.
Attachment 3
3-4
UNIT 2 EVENT TIMELINE
I
Clock Time
Event Time
Description
500 kV SWitchyard Red Bus Isolation Breakers 552-21 and 552-61
trip open, completing the high side isolation 13 kV Station Service
08:24:28:783 3.558 sec Transformer P-13000-2.
Undervoltage signal actuates on Unit 2 4 kV Vital Bus 24, initiating
08:24:29:451 4.226 sec
the 2B Emergency Diesel Generator start sequence.
Unit 2 4 kV Vital Bus 24 Normal Feeder Breaker 152-2401 trips
08:24:29:511 4.286 sec open.
Unit 2 automatic reactor trip on reactor coolant low flow signal from
100% initial reactor power level. All Unit 2 reactor coolant pumps
08:24:29:788 4.563 sec have stopped.
08:24:29 :827 4.602 sec Unit 2 reactor trip breakers open.
08:24:30:019 4.794 sec
Unit 2 turbine trip.
~Ta:897sec Emergency Diesel Generator 2B reaches 250 rpm.
13 kV Service Bus 21 Supply Breaker 252-2103 to Transformer U
108:24;33:818 8.593 sec 4000-22 opens.
13 kV Service Bus 21 Supply Breaker 252-2102 to Transformer U
08:24;33:818 8.593 sec
~OOO-21 opens.
13 kV Service Bus 21 Supply Breaker 252-2101 to Transformer U
08:24:33:819 8.594 sec 4000-23 opens.
08:24:33:889 8.664 sec 4 kV Non-Vital Bus 22 Feeder Breaker 152-2201 opens.
08:24:33:909 8.684 sec 4 kV Non-Vital Bus 23 Feeder Breaker 152-2311 opens.
08:24:35:988 10.763 sec Emergencv Diesel Generator 2B reaches 810-rpm.
Emergency Diesel Generator 2B Output Breaker 152-2403 to 4 kV
08:24:37:306 12.081 sec Vital Bus 24 closes.
08:24:37:785 12.560 sec 208/120 V/AC Bus 22 re-energizes.
08:24:37:887 12.662 sec Undervoltage signal clears on Unit 2 4 kV Vital Bus 24.
08:24:45:155 19.930 sec Emergency Diesel Generator 2B trips.
Emergency Diesel Generator 2B Output Breaker 152-2403 to 4 kV
08;24:45:185 19.960 sec Vital Bus 24 opens.
08:24:45:320 20.095 sec 208/120 V/AC Bus 22 de-energizes.
08:24:47:315 22.090 sec Undervoltage signal actuates on Unit 2 4 kV Vital Bus 24.
. 908 sec 21 and 22 Steam Generator Feed Pumps low suction pressure trip .
Reactor Operator backs up the automatic reactor trip signal by
1.110 sec depressing manual reactor trip pushbuttons.
08:24:55
30 sec
Crew enters EOP-O, Post-Trip Immediate Actions
Commenced boration because of loss of power to rod position
indication. Aligned gravity feed flowpath from boric acid storage
tanks to charging pump suction through 2-MOV-508 and 2-MOV
08:26
2min
509.
- Manually closed 2-MS-343, Main Steam (MS) Isolation to 22
'Moisture Separator Reheater (MSR) as altemate action because 2
08:32
8 min
iMS-4019-CV, MS to 22 MSR 2nd Stage failed to close.
Steam-driven AFW Pump 21 started to maintain SG heat sink,
08:33
9min
feeding approximately 150 gpm to each steam generator.
08:34
10min
2Y10 tied to 2Y09. Power restored to 2Y10.
Crew exits EOP-O and enters EOP-2, Loss of Offsile Power I Loss of
08:38
14 min
Forced Circulation
08:47
23 min
Report of smoke and acrid odor, vicinity of MCC-207
Attachment 3
3-5
UNIT 2 EVENT TIMELINE
Clock Time
Event Time
Description
08:53
29 min
Unit 2 main steam isolation valves closed.
4 kV Vital Bus 24 Alternate Feeder Breaker 152-2414 closed.
Shutdown sequencer is manually initiated per EOP Attachment 16.
08:57
33 min
The undervoltage signal clears on Unit 2 4 kV Vital Bus 24.
09:00
36 min
Restored Unit 2 CVCS letdown.
09:08
44 min
Low condenser vacuum.
.vCT Outlet MOV-501 opened. Boration stopped. Approximately
09:10
46 min
1936 gallons of boric acid injected.
!
Electricians report acrid odor coming from closed 4 kV Non-vital Bus
23 Supply Breaker 152-2501 (cause later diagnosed as a burnt
09:20
56 min
breaker trip coil).
10:46
2.37 hrs
Chemistry samples RCS for boron concentration.
Completed verification of required shutdown margin per NEOP-301 '
11:00
2.60 hrs
Attachment 3. Required concentration determined to be 1297_ppm.
Started 23 AFW Pump (motor-driven) and stopped 21 AFW Pump
111 :17
2.88 hrs
Ilturbine-driven).
Crew exits EOP-2 and enters OP-5, Plant Shutdown From Hot
11 :18
2.90 hrs
Standby to Cold Shutdown.
Chemistry reports RCS boron 1479 ppm. Initial concentration was
11:30
3.10 hrs
1129 ppm prior to the event.
11 :47
3.38 hrs
Completed 4 hr report to NRC, as required per 10CFR50.72.
,
12:11
3.78 hrs
Disconnects for 500 kV Switch yard Breaker 552-21 are opened.
i12:14
3.83 hrs
Disconnects for 500 kV Switchyard Breaker 552-61 are opened.
~.
3.85 hrs
Disconnects for 500 kV Switchyard Breaker 552-23 are opened.
12:17
3.88 hrs
Disconnects for 500 kV Switchyard Breaker 552-22 are opened.
12:18
3.90 hrs
Disconnects for 500 kV Switchyard Breaker 552-63 are opened.
Completed STP-O-90-2, AC Sources and Onsite Power Distribution
Systems 7 Day Operability Verification. This was a missed action
requirement of TS 3.8.1, required to be completed within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> of
12:55
4.52 hrs
the event.
Commenced RCS CooJdown # 87 using Natural Circulation to target i
113:30
5.10 hrs
temperature of 445°F per OP-5 to protect RCP seals.
IStopped RCS Cool down # 87 based on decision to start two RCPs
14:45
6.35 hrs
land gO on forced circulation. RCS temperature at 505°F.
17:13
8.82 hrs
Started 21 Band 22A RCPs. Forced RCS circulation restored.
21:50
13.43 hrs Disconnects for 500 kV Switchyard Breaker 552-22 closed.
22:00
13.60 hrs 500 kV Switchyard Breaker 552-22 closed.
22:01
13.62 hrs Disconnects for 500 kV Switchyard Breaker 552-23 closed.
22:07
13.72 hrs 500 kV Switchyard Breaker 552-23 closed.
02/19/2010
00:29
Started 21 Condensate Pump
02:56
Started 21 CirculatinQ Water Pump
Restored Gland Sealing Steam
Performed fast speed start test of EDG 2A
EDG 2A paralleled to 4 kV Bus 21.
07:49
A at full load on 4 kV Bus 21.
l10:08
ed SMECO to 13 kV Bus 21.
Attachment 3
i
UNIT 2 EVENT TIMELINE
Clock Time
Event Time
Description
11 :01
Energized U-4000-21 from 13 kV Bus 21 (SMECO feeding).
11 :02
Energized U-4000-22 from 13 kV Bus 21 (SMECO feeding).
Two offsite power sources verified OPERABLE with SMECO
12:05
27.6 hrs
supplying 13 kV Bus 21 and available to Unit 2 4 kV buses.
12:28
Unloaded EDG 2A.
12:32
Shutdown EDG 2A. Completed 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> loade'd test run.
Restored normal power supply alignment for 208/120 Instrument
13:52
Bus 22 (2Y10). 2Y09 and 2Y10 are un-tied.
02120/2010
17:19
57 hrs
Performed fast speed start test of EDG 2B.
17:36
EDG 2B paralleled to 4 kV Bus 24.
17:46
EDG 2B at full load on 4 kV Bus 24.
21:57
Unloaded EDG 2B.
22:02
Shutdown EDG 2B. Completed 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> loaded test run.
22:31
62 hrs
02/21/2010
04:24
Commenced drawing main condenser vacuum.
05:50
69.5 hrs
Divorced from SMECO, re-energized 500 kV Red Bus.
09:24
Opened 21 and 22 Main Steam Isolation Valves
09:25
73 hrs
Recommenced RCS Cooldown # 87 to MODE 5 per OP-5.
17:16
81 hrs
Unit 2 in MODE 4, RCS temperature < 350°F.
20:12
84 hrs
Stopped RCS cooldown to degas RCS.
02/2212010
01:30
89 hrs
Recommenced RCS cooldown.
05:00
92.6 hrs
Unit 2 in MODE 5, RCS temperature < 200°F.
Attachment 3