ML042960506

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Augmented Inspection Team Exit Meeting with Palo Verde Nuclear Generation Station
ML042960506
Person / Time
Site: Palo Verde  Arizona Public Service icon.png
Issue date: 10/18/2004
From:
NRC Region 4
To:
References
FOIA/PA-2004-0307
Download: ML042960506 (15)


Text

Nuclear Regulatory Commission Augmented Inspection Team Exit Meeting with Palo Verde Nuclear Generation Station

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Inspection Charter

  • Basis of Augmented Inspection
  • Develop a complete sequence of events
  • Assess performance of plant systems
  • . Assess adequacy of plant procedures

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I MF*.Wfm Inspection Charter

    • Assess facility response to event
  • Assess facilities determination of apparent cause

+.* Assess maintenance related contributions

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Inspection Charter

  • . Assess facility coordination of offsite activities
    • Overall risk assessment of event

I-s SEQUENCE OF EVENTS

  • Fault Initiation
  • . Electrical Transmission and Grid

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  • s SEQUENCE OF EVENTS
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Other Challenges

A-N PERFORMANCE OF PLANT SYSTEMS

  • .* Transmission system protection
  • .* All three reactors were safely shut down
  • Each unit was stabilized by operators

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PERFORMANCE OF PLANT SYSTEMS

  • .+.Other minor equipment problems noted during shutdown

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Plant Procedures

  • . Procedures used during event were generally acceptable
    • Some issues noted

MMW Facility Response

  • Conduct of operations generally good
  • . Emergency response organization challenges
  • Some other problems noted by the team

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j7:;ji Apparent Causes

-. Electrical fault isolation failure

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Transmission lines between Hassayampa and Palo Verde switchyard

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Technical Support Center Emergency Diesel Generator failure

    • Others

Maintenance Related Aspects

  • Maintenance of switchyard and substation equipment good
  • . Implementation of facility maintenance processes

SUEDAMINOs A.C Off-Site Coordination

  • . Good coordination of actions following event
  • t Unrecognized design issue with Hassayampa to Palo Verde transmission line protection

Overall Risk Assessment

    • Given the loss of approximately 5,500 MWe of electrical generation, the grid performed well
  • Electrical power was restored in a timely*

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Overall Risk Assessment

    • All three units were stabilized and placed in a safe shutdown mode of operation