ML020370079

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December 2001 Monthly Operating Report for Beaver Valley Power Station, Units 1 & 2
ML020370079
Person / Time
Site: Beaver Valley
Issue date: 01/08/2002
From: Myers L
FirstEnergy Nuclear Operating Co
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
GL-97-002, L-02-002
Download: ML020370079 (5)


Text

FENOC "F'rstEnargy Ntxaar Operating Cornpanry L-02-002 January 8, 2002 Beaver Valley Power Station Unit I - Docket No. 50-334, License No. DPR-66 Unit 2 - Docket No. 50-412, License No. NPF-73 Monthly Operating Report U. S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555 Gentlemen:

In accordance with NCR Generic Letter 97-02, "Revised Contents of the Monthly Operating Report," and Unit I and 2 Technical Specification 6.9.4, the "Monthly Operating Report" is submitted for Unit I and Unit 2 for the month of December 2001.

Respectfully, Lew W. Myer(

Senior Vice-P ident - Nuclear DTJIhkh Enclosures C:

NRC Regional Office King of Prussia, PA

UNIT SHUTDOWNS DOCKET NO.

50-334 UNIT NAME BVPS Unit #1 DATE January 3, 2002 COMPLETED BY David T. Jones TELEPHONE (724) 682-4962 REPORTING PERIOD:

December 2001 No.

Date Type Duration Reason Method of Cause / Corrective Actions (DIM/Y)

F: Forced (Hours)

(1)

Shutting S: Scheduled Down (2)

Comments 6

071201 F

59.4 H

2 While at 100% output, the Reactor was manually tripped due to loss of station air pressure. The loss of station air pressure occurred when the 1A Station Air Compressor tripped while the 1 B Station Air Compressor was out of service for preventive maintenance (PM) work. The PM required verification that all wiring terminations associated within the control panel for the compressor were tight. While checking the connections, a short occurred when a screwdriver without insulation was used to tighten a terminal screw. The short grounded the control circuit for an interconnection with the 1A Station Air Compressor, causing it to blow a control power fuse. This interconnect was not clearly evident in the PM work order. The blown control power fuse caused the 1 A Station Air Compressor to trip. Trip of compressor 1 A combined with the tag-out and work being performed on compressor 1B, caused loss of station air pressure, forcing a manual trip of the Reactor.

(1) Reason (2) Method A - Equipment Failure (Explain) 1 - Manual B - Maintenance or Test 2 - Manual Trip Scram C - Refueling 3 - Automatic Trip I Scram D - Regulatory Restriction 4 - Continuation E - Operator Training / License Examination 5 - Other (Explain)

F - Administrative G - Operational Error (Explain)

H - Other (Explain)

SUMMARY

The Unit began the report period operating at a nominal value of 100% output. On 12/7/01 at 1401 hours0.0162 days <br />0.389 hours <br />0.00232 weeks <br />5.330805e-4 months <br />, the Reactor was manually tripped due to loss of station air pressure. The Unit was stabilized in Mode 3 while the cause and evaluation of the trip continued (see above for details). Upon determination that startup could proceed, the Unit commenced Reactor startup, entering Mode 2 at 1656 hours0.0192 days <br />0.46 hours <br />0.00274 weeks <br />6.30108e-4 months <br /> and going critical at 2023 hours0.0234 days <br />0.562 hours <br />0.00334 weeks <br />7.697515e-4 months <br /> on 12/9/01.

The Unit was synchronized to the electrical grid at 0126 hours0.00146 days <br />0.035 hours <br />2.083333e-4 weeks <br />4.7943e-5 months <br /> on 12/10/01, achieving a nominal value of 100%

output at 1730 hours0.02 days <br />0.481 hours <br />0.00286 weeks <br />6.58265e-4 months <br /> on 12/10/01.

The Unit continued to operate at a nominal value of 100% output for the remainder of the report period.

OPERATING DATA REPORT REPORTING PERIOD:

DECEMBER 2001 DESIGN ELECTRICAL RATING (Net MWIe):

MAX.

DEPENDABLE CAPACITY (Net MWe):

DOCKET NO.:

50-334 UNIT NAME:

BVPS UNIT #1 REPORT DATE:

01/03/02 COMPLETED BY:

DAVID T.

JONES TELEPHONE:

(724) 682-4962

  • Notes:

Rated thermal power at

  • BVPS-l was uprated from 2652 MWt*

835

  • to 2689 MWt on 10/20/01.

Net

  • MDC was also uprated from 821
  • 810 MWe to 821 NWe.

HOURS IN REPORTING PERIOD:

NO.

OF HRS.

REACTOR WAS CRITICAL:

SERVICE HOURS GENERATOR ON LINE:

UNIT RESERVE SHUTDOWN HOURS:

NET ELECTRICAL ENERGY GEN.

(MWH):

GROSS ELECT.

ENERGY GEN.

(MWH):

GROSS THERMAL ENERGY GEN.

(MWH):

UNIT AVAILABILITY FACTOR (%):

UNIT CAPACITY FACTOR (MDC)

(M):

UNIT FORCED OUTAGE RATE (M):

THIS MONTH 744.0 689.6 684.6 0.0 564958.0 599918.0 1823296.0 92.0 92.5 8.0 YEAR TO DATE 8760.0 7461.6 7409.7 0.0 5991023.0 6356373.0 19327289.0 84.6 84.2 2.8 CUMULATIVE 225024.0 152081.5 149621.9 0.0 111666143.0 119266786.0 367634805.5 67.9 63.2 16.4 la.

1.

2.

3a.

3.
4.
5.
6.
7.
8.
9.
10.

II.

UNIT SHUTDOWNS DOCKET NO.

50-412 UNIT NAME BVPS Unit #2 DATE January 3, 2002 COMPLETED BY David T. Jones TELEPHONE (724) 682-4962 REPORTING PERIOD:

December 2001 No.

Date Type Duration Reason Method of Cause / Corrective Actions (D/M/Y)

F: Forced (Hours)

(1)

Shutting S: Scheduled Down (2)

Comments NONE.

(1) Reason (2) Method A - Equipment Failure (Explain) 1 - Manual B - Maintenance or Test 2 - Manual Trip I Scram C - Refueling 3 - Automatic Trip / Scram D - Regulatory Restriction 4 - Continuation E - Operator Training / License Examination 5 - Other (Explain)

F - Administrative G - Operational Error (Explain)

H - Other (Explain)

SUMMARY

The Unit operated at a nominal value of 100% output for the entire report period.

OPERATING DATA REPORT DOCKET NO.:

UNIT NAME:

REPORT DATE:

COMPLETED BY:

TELEPHONE:

REPORTING PERIOD:

DECEMBER 2001 DESIGN ELECTRICAL RATING (Net MWe):

MAX.

DEPENDABLE CAPACITY (Net MWe):

836 831 50-412 BVPS UNIT #2 01/03/02 DAVID T.

JONES (724) 682-4962 Notes: Rated thermal power at BVPS-2 was uprated from 2652 MWt*

to 2689 Mwt on 10/30/01.

Net MDC was also uprated from 820 MWe to 831 MWe.

HOURS IN REPORTING PERIOD:

NO.

OF HRS.

REACTOR WAS CRITICAL:

SERVICE HOURS GENERATOR ON LINE:

UNIT RESERVE SHUTDOWN HOURS:

NET ELECTRICAL ENERGY GEN.

(MWH):

GROSS ELECT.

ENERGY GEN.

(MWH):

GROSS THERMAL ENERGY GEN.

(MWH):

UNIT AVAILABILITY FACTOR (M):

UNIT CAPACITY FACTOR (MDC)

(%6):

UNIT FORCED OUTAGE RATE (96):

THIS MONTH 744.0 744.0 744.0 0.0 631976.0 664863.0 1997250.0 100.0 102.2 0.0 YEAR TO DATE 8760.0 8712.1 8702.6 0.0 7191653.0 7567068.0 22689519.0 99.3 99.9 0.7 CUMULATIVE 123807.0 101354.5 100692.6 0.0 78578092.0 83074743.0 253407581.0 81.3 77.0 10.4 la.

1.

2.

3a.

3.
4.
5.
6.
7.
8.
9.
10.

i1.