LR-N02-0396, October 2002 Monthly Operating Report for Hope Creek Generating Station

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October 2002 Monthly Operating Report for Hope Creek Generating Station
ML023250399
Person / Time
Site: Hope Creek PSEG icon.png
Issue date: 11/13/2002
From: Garchow D
Public Service Enterprise Group
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
LR-N02-0396
Download: ML023250399 (3)


Text

PSEG Nuclear LLC P.O Box 236, Hancocks Bridge, New Jersey 08038-0236 NOV 1 3 20O2 LR-N02-0396 O PSEG Nuclear LLC U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:

MONTHLY OPERATING REPORT HOPE CREEK GENERATING STATION DOCKET NO. 50-354 In compliance with Section 6.9, Reporting Requirements for the Hope Creek Technical Specifications, the operating statistics for October 2002 are being forwarded.

Sincerely, D. F. Garchro Vice Presidye-(Operations RAR Attachments C Distribution 1/2 95-2168 REV 7/99 B

DOCKET NO.:

UNIT:

DATE:

COMPLETED BY:

TELEPHONE:

50-354 Hope Creek 11/12/02 F. Todd (856) 339-1316 Reporting Period October 2002 I

OPERATING DATA REPORT Design Electrical Rating (MWe-Net)

Maximum Dependable Capacity (MWe-Net)

No. of hours reactor was critical No. of hours generator was on line (service hours)

Unit reserve shutdown hours Net Electrical Energy (MWH) 1083 1049 Month Y ear-to-aaie koumuiaxive 745 7229 119651 745 7090 117355 0

0 0

776241 7266586 118902194 UNIT SHUTDOWNS NO.

DATE TYPE DURATION REASON METHOD OF CORRECTIVE ACTION/

F=FORCED (HOURS)

(1)

SHUTTING COMMENT S=SCHEDULED DOWN THE REACTOR (2)

(1) Reason (2) Method A - Equipment Failure (Explain)

B - Maintenance or Test C - Refueling D - Regulatory Restriction E - Operator Training/License Examination F - Administrative G - Operational Error (Explain)

H - Other 1 - Manual 2 - Manual Trip/Scram 3 - Automatic Trip/Scram 4 - Continuation 5 - Other (Explain)

DOCKET NO.: 50-354 UNIT: Hope Creek DATE: 11/12/02 COMPLETED BY: R. Ritzman TELEPHONE: (856) 339-1445 Summary Of Monthly Operating Experience

  • On October 26, power was reduced to approximately 62% for a Deep Shallow Rod Swap. During the Deep Shallow Rod Swap evolution, a tube leak in the "C" waterbox was repaired. Power was restored to approximately 100% on October
27.
  • At the end of the month, Hope Creek completed 126 days of continuous on-line operation.