05000387/LER-2016-018, Regarding Inoperability of RCIC Due to an Oil Leak

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Regarding Inoperability of RCIC Due to an Oil Leak
ML16173A392
Person / Time
Site: Susquehanna Talen Energy icon.png
Issue date: 06/21/2016
From: Franke J
Susquehanna, Talen Energy
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
PLA-7497 LER 16-018-00
Download: ML16173A392 (4)


LER-2016-018, Regarding Inoperability of RCIC Due to an Oil Leak
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded

10 CFR 50.73(a)(2)(viii)(A)

10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition

10 CFR 50.73(a)(2)(viii)(B)

10 CFR 50.73(a)(2)(iii)

10 CFR 50.73(a)(2)(ix)(A)

10 CFR 50.73(a)(2)(iv)(A), System Actuation

10 CFR 50.73(a)(2)(x)

10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor

10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat

10 CFR 50.73(a)(2)(v), Loss of Safety Function

10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown

10 CFR 50.73(a)(2)(vii), Common Cause Inoperability

10 CFR 50.73(a)(2)(i)
LER closed by
IR 05000387/2016004 (10 February 2017)
3872016018R00 - NRC Website

text

JUN 2 1 2016 Jon A. Franke Susquehanna Nuclear, LLC Site Vice President 769 Salem Boulevard Berwick, PA 18603 Tel. 570.542.2904 Fax 570.542.1504 Jon.Franke@TalenEnergy.com U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555-0001 SUSQUEHANNA STEAM ELECTRIC STATION LICENSEE EVENT REPORT 50-387/2016-018-00 UNIT 1 LICENSE NO. NPF-14 PLA-7497 TALEN~

ENERGY 10 CFR 50.73 Docket No. 50-387 Attached is Licensee Event Report (LER) 50-387/2016-018-00. The LER reports an event involving inoperability of Reactor Core Isolation Cooling (RCIC). This event was determined to be reportable in accordance with 10 CFR 50.73(a)(2)(i)(B) as a condition prohibited by Technical Specifications.

There were no actual consequences to the health and safety of the public as a result of this event.

This letter contains no new regulatory commitments.

J. A. Franke Attachment: LER 50-387/2016-018-00 Copy:

NRC Region I Mr. J. E. Greives, NRC Sr. Resident Inspector Ms. T. E. Hood, NRC Project Manager Mr. M. Shields, PA DEP/BRP

NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31/2018 (11 -2015)

, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

3. PAGE Susquehanna Steam Electric Station Unit 1 05000387 1 of 3
4. TITLE lnoperability of RCIC Due to an Oil Leak
5. EVENT DATE
6. LER NUMBER
7. REPORT DATE
8. OTHER FACILITIES INVOLVED YEAR I SEQUENTIAL I REV FACILITY NAME DOCKET NUMBER MONTH DAY YEAR NO.

MONTH DAY YEAR 05000 NUMBER FACILITY NAME DOCKET NUMBER 04 22 2016 2016

- 018
- 00 0/.o.Q..l 2016 05000
9. OPERATING MODE
11. THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §:(Check all that apply)

D 20.2201(b)

D 20.2203(a)(3)(i)

D 50.73(a)(2)(ii)(A)

D 50.73(a)(2)(viii)(A) 1 D 20.2201(d)

D 20.2203(a)(3)(ii) 0 50.73(a)(2)(ii)(B)

D 50.73(a)(2)(viii)(B)

D 20.2203(a)(1)

D 20.2203(a)(4)

D 50.73(a)(2)(iii)

D 50.73(a)(2)(ix)(A)

D 20.2203(a)(2)(i) 0 50.36(c)(1)(i)(A)

D 50.73(a)(2)(iv)(A)

D 50.73(a)(2)(x)

D 20.2203(a)(2)(ii)

D 50.36(c)(1 )(ii)(A)

D 50.73(a)(2)(v)(A)

D 73.71 (a)(4)

10. POWER LEVEL D 20.2203(a)(2)(iii)

D 50.36(c)(2)

D 50.73(a)(2)(v)(B)

D 73.71 (a)(5)

D 20.2203(a)(2)(iv)

D 50.46(a)(3)(ii)

D 50.73(a)(2)(v)(C)

D 73.77(a)(1) 010 D 20.2203(a)(2)(v) 0 50.73(a)(2)(i)(A)

D 50.73(a)(2)(v)(D)

D 73.77(a)(2)(i)

D 20.2203(a)(2)(vi)

~ 50.73(a)(2)(i)(B)

D 50.73(a)(2)(vii)

D 73.77(a)(2)(ii) 0 50.73(a)(2)(i)(C) 0 OTHER Specify in Abstract below or in

, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

2. DOCKET NUMBER
3. LER NUMBER YEAR I

SEQUENTIAL I

REV NUMBER NO.

05000387 2016

- 018
- 00 Based on the leakage identified on April 16, 2016 and the subsequent leakage identified on April 22, 2016 that was sufficient to require declaring RCIC inoperable, RCIC is considered to have been inoperable prior to mode change. As a result, the condition is considered to be a violation of Technical Specification 3.0.4 and reportable in accordance with 10 CFR 50.73(a)(2)(i)(B) as a condition prohibited by Technical Specifications.

CAUSE OF EVENT

Cause information will be provided in a supplement to this LER.

ANALYSIS/SAFETY SIGNIFICANCE

Evaluation of the safety significance will be provided in the planned supplement to this LER.

CORRECTIVE ACTIONS

Key corrective actions include the following:

1. The oil leak was repaired.

COMPONENT FAILURE INFORMATION

Information will be provided in the supplement to this LER.

PREVIOUS SIMILAR EVENTS

Previous similar events will be provided in the supplement to this LER.

NRC FORM 366 (11-2015)