Similar Documents at Cook |
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LER-2076-043, Re Failure of S/G Level Transmitter |
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| 3162076043R00 - NRC Website |
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Ki<C I.OIP:,i 106 V.S. IIVCLEAilIlCGVLATOBY<
AISSION p 76I
'NFIC DISTRIBUTION roB 'PART 50 DOCKET'MATERIAL DOCKET NUMIIEQ W~3 /E FiLE NVI.IIIEB XliCXDENT HI.""PORT TO:
Indiana-6 Michigan Pwr Co Mr Keppler I-ROM:
Indiana 6 Michigan Pwr 'Co Bridgman, Michigan R W Jurgensen.
DATL OI'OCUMENT 10-14-76 DATC RECEIVED 10-19-8'6
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COPY DCSCFIIPTION,,
ONOTOBIZED NCLASSIFIED PROP INPUT I-OBM CNCLOSV BE NUMIIEB OF COP ICS RECEIVED lcc Ltr trans the following:
PIANT NAIVE.
Cook yg Licensee Event Report (R)876-43) on 9-13-76 concerning failure of the S/G level transmitt
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iVDIAIVA8 MICH 8AN POPOVER CO III DONALD C. COOK NUCLEAR PLANT P.O. Box 458, Bridgman, Michigan 49106 October 14, 1976 Nr. J.G.
- Keppler, Regional Director Office of Inspection and Enforcement United States Nuclear Regulatory Commission Region III 799 Roosevelt Road Glen Ellyn, IL 60137
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QCT19 19761 9
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Dear Nr. Keppler:
Operating License DPR-58 Docket No. 50-315 Pursuant to the requirements of Appendix A Technical Specifications and the United States Nuclear Regulatory Commission Regulatory Guide
- 1. 16, Revision 4, Section 2.b, the following report, is submitted:
'RO 50-315/76-'43.
Sincerely,
.W. Jurg en Plant Ma ger
/bab CC:
R.S.
Hunter J.E.
Dolan G.E. Lien R. Kilburn R.J.
Yollen BPI R.C. Callen NPSC K.R. Baker RO:III R. Walsh, Esq.
P.W. Steketee, Esq.
G. Charnoff, Esq.
G. Olson J.M. Hennigan PNSRC R.S.
Keith Dir., IE (30 copies)
Dir.,
MIPC (3 copies) i.OSV9
[oO~J M
es CONTROL BLOCK:~
UCENSEE NAME I
.D CC 1
0 0
14 15 UCENSE NUMBER 0
0 0
0 0 0 0
SE PRNIT ALLRMUIAEO INPQRIVIA UCENSE EVENT TYPE TYPE 4
I I
I I
~03 26 30 31 32 REPORT REPOAT CATEGORY TYPE SOURCE [OD1]CON'T~
7 8
57 58 59 60 61 DOCKET NUMBEA EVENT DATE REPORT DATE 0
9 1.
3 7
6 1
0 1
4 7
6 68
, 69 74 75 BQ EVENT OESCRIPTION QP2 WHILE IN MODE 5 DURING THE PERFORMANCE OF A SURVEILLANCE TEST, THE S/G LEVEL TRANS" 7
8 9 [QQ3f MITTER (BLP-120)
WAS 104 1255 IN EXCESS OF THE TECH SPEC LIMIT AS OUTLINED IN TABLE 7
89 toad 2 2-1 7
8 9 Jog ao aa 7
8 9 Jog (RO 50-315/76-43) 80 7
8 9 SYSTEM
CAUSE
CODE CODE COMPONENT CODE [oar] ~IE
~E I
N S
T' 7
8 9 10 11 12 CAUSE OESCRIPTION 55 I
ES FAME COMPONENT SUPPUEA 17 43 44 COMPONENT MANUFACTUAEA 47 7
8 9 [os WAS A REOCCURRENCE OF THE ZERO SHIFT.
THE FOXBORO TRANS 7
8 9
~1o WAS REBUILT, REPLACI'NG THE AMP ¹N014354 AND THE F 80 80 80.
N0150MA SEE SUPPLEMENT OTHER STATUS 7
8 9 LOSS OR OAMAGE TO FACIUTY TYPE
DESCRIPTION
~6
~Z NA 7
89 10 PUBUCITY
~17 NA 7
8 9 AOOITIONAL FACTORS Q~g NA 7
89 Q~g NA 7
89 NAME.J. L. RISCHLING 7
89, FACNlTY STATUS TG POWER G
~00 0
NA 7
8 9
10 12 13 FOAM OF ACTIVITY CO@TENT RELEASED OF RELEASE.
AMOUNT OF ACTIVITY l112 Z
Z NA
~ 7 8
9 10 11 PERSONNEL EXPOSUFIES NUMBER TYPE OESCRNollON
'ig ~00 0
~Z NA 7
89 11 12 13 PERSONNEl.
INJURIES NUMBER
DESCRIPTION
~44 ~00
'0 NA 7
89 11 12 PROBABLTE CONSEQUENCES Qsg NA 44 45 NA METHOD OF DISCOVERY B
44 45 46 DISCOVERY OESCSPTION SURVEILLANCE TEST LOCATION OF RELEASE PHQN$ 616 465-5901 368) ao 80 ao 80 BQ ao ao 80 aO GPO ddf dd'F
1 SUPPLEMENT TO REPORTABLE'OCCURRENCE'RO-50-315 76-43 SUPPLEMENT TO CAUSE DESCRIPTION THE TRANSMITTER WAS CALIBRATED AND TESTED, THE INSTRUMENT FUNCTIONED PROPERLY WITH NO ZERO SHIFT.
THE TRANSMITTER WAS RECALIBRATED AND RETURNED TO SERVICE.
gb,me~n NDIANA& MICHIGANPDNE'R GD DONALD C. COOK NUCLEAR PLANT P.O. Box 458, Bridgman, Michigan 49106 October 14, 1976 Mr. J.G.
- Keppler, Regional Director Office of Inspection and Enforcement United States Nuclear Regulatory Commission Region III 799 Roosevelt Road Glen Ellyn, IL 60137
Dear Mr. Keppler:
Operating License DPR-58 Docket No. 50-315 Pursuant to the requirements of Appendix A Technical Specifications and the United States Nuclear Regulatory Commission Regulatory Guide
- 1. 16, Revision 4, Section 2.b, the following report is submitted:
RO 50-315/76-43.
Sincerely,
.W. Jurg en Plant Ma ger
/bab cc:
R.S.
Hunter J.E.
Dolan G.E. Lien R. Kilburn R.J. Vollen BPI R.C. Callen MPSC K.R. Baker RO:III R. Walsh, Esq.
P'.W. Steketee, Esq.
G. Charnoff, Esq.
G. Olson J.M. Hennigan PNSRC R.S.
Keith Dir., IE (30 copies)
Dir., MIPC (3 copies)
OCT 19 1976
7 t)I)tp a
y p a
CONTROL BLOCK LICENSEE EVENT REPORT f
SE PRINT ALLREQUIRED INFORIVIATION7 1
6 UCENSEE NAME LICENSE NUMBER jopj M
I 0
CC 1
0 0
0 0
0 00 7
89 14 15 REPORT REPORT CATEGORY TYPE SOURCE OOCKET NUMBER Iaaf cow~~
7 8
57 58 59 60 61 EVENT TYPE UC ENSE TYPE 0
0 4
1 1
1 1
L0003~I 25 26 30 31 32 EVENT OATE REPORT OATS 0
9 1
3 7
6 1
0 1
4 7
6 68
. 69 74 75 80
EVENT DESCRIPTION
[oO~J WHILE IN MODE 5, DURING THE PERFORMANCE OF A SURVEILLANCE TEST, THE S/G LEVEL TRANS-7 8 9 [QQ3]
MITTER (BLP-120)
WAS 10. 12M IN EXCESS OF THE TECH SPEC LIMIT AS OUTLINED IN TABLE 7
89 gQ 2.2-1.
7 8 9 80 80 80 80 7
8 9 [oaf (RO 50-315/76-43)
~ 80 7
8 9 SYSTEM COOE FAME COMPONENT SUPPUER COMPONENT MANUFACTURER
CAUSE
COOE COMPONENT COOE Ioc>I Lii~J
~E I
N 3 1
R 7
8 9 10 11 12 CAUSE DESCRIPTION Qg IN E
17 43 47 48 80 80 N0150MA SEE SUPPLEMENT 80 7
89 FACILITY STATUS
% POWER
~G
~00 0
NA 7
8 9
10 12 13 FORM OF 7
8 9
10 11 PERSONNEL EXPOSURES NUMBER TYPE OESCRIPTION Q~g ~00 0
~Z NA 7
8 9 11 12 13 PERSONNEL INJURIES NUMBER OESCRIPTION
~>4 ~00 0
NA 7 89'1 12 PROBABLE CONSEQUENCES
~15 NA METHOO OF OISCOVERY OISCOVERY OESCRIPTION OTHER STATUS SURVEILLANCE TEST B
44 45 46 80 LOCATION OF RELEASE AMOUNT OF ACTIVITY NA 44 45 80 80 80 7
8 9 t00js WAS A REOCCURRENCE OF THE ZERO SHIFT.
THE FOXBORO TRANSM T as
~so WAS REBUILT, REPLACING THE AMP IIIN014354 AND T E
7 8 9 LOSS OR DAMAGE TO FACIUTY TYPE OESCRIPTION
~16 Z
NA 7
89 10 PUBLICITY NA 7
89 ADDITIONAL FACTORS NA 7
8 9 NA 7
89 NAME'.J. L. RISCHLING PHDN$616 465-5901 368) 80 80 80 80 80 GPO 001 ~ 001
SUPPLEMENT TO REPORTABLE 'OCCURRENCE 'RO-50-315 76-43 SUPPLEMENT TO CAUSE DESCRIPTION THE TRANSMITTER WAS CALIBRATED AND TESTED, THE INSTRUMENT FUNCTIONED PROPERLY WITH NO ZERO SHIFT.
THE TRANSMITTER WAS RECALIBRATED AND RETURNED TO SERVICE.
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| | | Reporting criterion |
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