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t Florida Power C 0 R P O R AT t O N.
Crystal River Unit 3
- - Docket No. 50-302 April 27, 1992 3F0492-12
- - U. S. Nuclei. Regulatory Commission
. Attention:- ']cument Control Desk Washington, D.'C.
20555
Subject:
Licensee Event Report (LER)'92-01
Dear Sir:
Enclosed is Licensee Event Report (LER) 92-01 which is submitted in
- - accordance with 10 CFR-50.73.
. Sincerely,
'G. L. Boldt Vice President Nuclear Production
~EEF: mag:
Enclosure
<xc:.-Regional-Administrator, Region,Il ProjectLManager,:NRR-Senior Resident-Inspector.
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CRYSTAL river UNIT 3 (CR-3) o\\ slo lol o} 3l ol 2 ol2 olol1 ojo ol3hflol5 text y
-.-.au wmer.-=.m The reactor was stabilized in MODE 3, Hot Standby. The OP1 was checked, re-powered, and the ES busses returned to normal alignrnent. The Diesel Generators were secured.
The plant ns cooled down to MODE 5 for maintenance work on control rod position indication prior to post-trip restart.
A four hour report was made as required by 10CFR50.72(b)(2)(ii). This event is reportable under 10 CFR 50.73(a)(2)(iv).
CAUSE
The root cause of this event was relay design combined with the specific off-normal alignment of equipment utilized in the troubleshooting effort. Failed components in the inverter may have additionally contributed to the event.
The emergency power scheme for Crystal River 3 incorporates several levels of power sousces, one of these being four uninterruptible power supplies (UPS) [EE,UJX] called the Vital Busses.
Each 120 volt AC bus is powered from two sources, the preferred being the Vital Bus Static Inverter [EE.INVT] (a dual input inverter), end the alternate source being the 480 volt ES bus via a dedicated voltage regulating transformer which bypasses the inverter.
The inverter normally rectifies 480 volt ES AC power to DC power. The inverter then invertc the DC power back to 120 volt AC power, through a constant voltage transformer (EE,XFMR] within the inverter, which supplies the load, if the AC power input is lost, the inverter will instantly draw power from banks of lead-acid batteries [EE,BTRY] providing DC power and invert that to 120 volt AC power for the Vital busses.
At the beginning of this event, the 'C' Vital bus was being supplied from the alternate source, the 480 volt ES bus and voltaga regulating transforreer. because the normal ~ source, the inverter, was out
>..ervice for maintenance.
Under the troubleshooting package, several test configurations were to be established in the inverter to locate the root cause of the problem. A test corfiguration required that the Constant Voltage Transfcrmer [EE,XFMR], withir the inverter, be isolated by lifting the transformer leads. The inverter was then to be connected to ihe DC power input by closing the DC inpui. breaker. In the process of isplating the transformer, the electricians had only lifted one lead.
While this did take it out of the circuit, it did not isolate the transformer. When the DC input breaker was closed, y
tne partf ally isolated transformer induced an AC voltage (350 volts peak-to-peak)
L cnto the DC bus. The only apparent effect was the tripping of the icterposing relays used for normal 0PT feeder breaker control.
later testing showed a unique sensitivity in these relays, not shared generically threaghout the DC power system. The relay act Wa isolated the transformer and de-powered both ES 4160 volt busses. The loss c u bus power caused the EDGs to start.
NHC Form WeA (6-49)
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- 1 W #PJ OF MANAGEMENT Areo BUDGET, VeASPENGTON DC 20603.
FACUTY NAME (O DOET NUMBER p)
LER NUWGER $8)
PAGECD SEQUENTIAL R4MFIN CRYSTAL RIVER UNIT 3 (LR-3) ol sl ol Jl ol 3l ol 2 ol2 o l ol 1l-o l 0 o l 4 lCFl o f 5 rw,, _. n m m.on M NT EVALUATION:
There were four main consequences of the loss of ES busses: first, both EDGs started en a valid undervoltage signal on the ES 4160 volt busses. Second, the motor driven Emergency Feedwater Pump (EFWP) auto started on ES bus undervoltage and EDG output breaker closure.
Third, there vas no power to the
'C' Vital Bus because it was normally aligned to the "A" " 4160 volt bus /"A";ES 480 volt bus.
Fourth, due to electrical alignment and effected busses, there was no power to the CRD motors and all control = rods inserted on loss of power. Each of these consequences is discussed below.
j The loss of power to the ES 4160 volt bu*ses is a'ccounted for'in the~ design of the plant. Should ~ power be lost to the busses, the EDGs auto start, come to synchronous speed and automatically power the ES bus loads. This action occurred as expected.
The EDGs carried the ES 4160 bus loads until 1538 for the "B" EDG and until 1918 for the "A" EDG. The only anomaly in EDG performance was a leak in the Jacket cooling
- - system for the 'B' diesel.
The EFWP auto started, though there was no Emu jency Feedwater Initiation and Control (EFIC) system actuation. This is as designed.
Terever there is an undervoltage on the ES 4160 volt busses followed by an EDG output breaker closure, the motor driven EFP (EFP-1) auto starts as the bus is block loaded by the EDG. The EFIC system and
'EFP-1 both worked as designed and expected.
The 'C' vital: bus was deenergized because it was being fed by the ES 4160 volt bus /ES
- - 480 volt hus.
This bu: powers the 'C' Chaisnel of the Reactor Protection System (RPS). When the power to the syste r fails, the channel trips.
In addition to the RPS, channel "C",
the "C" Vital Bus also powers the Recall system, a passive data recording system, and an annunciator events recorder.
The loss of power caused a less of some transiant information normally used to analyze an event.
The CP,D motors lost power and all the control rods inserted into the core. The CRD motors are designed so that a sectioned roller nut engages a lead screw on the control rod. ~ The roller nut sections are designed to be disengaged from tht lead screw by springs. The roller nut is held in the engaged position by electromagnetic form. The roller nut is turned by progressing the electromagnetic field around the contul rod (moving in discrete steps), turning the roller nuts around the lead screw, raising and lowering the rod in the core. When power was lost to the CRD motors, the roller nuts disengaged and the rods inserted.
"NRCFORM3eM.
U.S. NUCLEAR HEGLAATORY COMutseeON APP 50VED OMJ N'l 31M104 EXPIRES 4/30/92 l
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RIVER UNIT 3 (CR-3)
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_. -. -, -.on CORRECTIVE ACT11NSt There were several corrective actions taken to preclude recurrence of this event.
Prior to plant restart, the relays that send the remote open signal to the feeder breakers for the OPT were disabled.
These relays provided no protective relaying
- - functions so-there. is no loss of equipment protection. The feeder breakers can now
.be manually opened with control switches installed in the 230 KV switchyard prior to startep.
A second action to monitor the DC bus for noise prior to reduced RCS inventory ' operations will be implement J during the upcoming ' refueling outage.
Lastly, a numan performance review will be conducted on the inverter troubleshooti.ng evolution to determine if the risks should have been known or anticipated. The first action _is already completed, the others are schedu}ed for completion _by July 1,1992.
PREVIOUS SIMILAR OCCURRENCESi
- - A 'similar actuation of these relays occurred during the mid-cycle 8 mai. tenance outage.
See LER 91-10 for details of that event.
J NHC Form 3a.A (6-49)
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| 05000302/LER-1992-001, :on 920327,inverter Output Connected to Dc Sys Input Isolated,Causing Two Relays to Actuate & Opening Feeder Breakers.Caused by Relay Design & Failed Components in Relays.Relays Disabled & Dc Bus Monitored |
- on 920327,inverter Output Connected to Dc Sys Input Isolated,Causing Two Relays to Actuate & Opening Feeder Breakers.Caused by Relay Design & Failed Components in Relays.Relays Disabled & Dc Bus Monitored
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000302/LER-1992-002, :on 920327,leakage from Seal of Jacket Coolant Pump DJP-2 Increased to Approx 2-3 Gallons Per Minute.Caused by Inoperable EDG & Vital Bus Inverter.Leak Repaired & Preventive Maint Program Modified |
- on 920327,leakage from Seal of Jacket Coolant Pump DJP-2 Increased to Approx 2-3 Gallons Per Minute.Caused by Inoperable EDG & Vital Bus Inverter.Leak Repaired & Preventive Maint Program Modified
| 10 CFR 50.73(a)(2)(1) | | 05000302/LER-1992-003-03, :on 910801,determined That Two Procedures for Documenting Vol of Fuel Stored in DG Fuel Oil Storage Tank Erroneously Revised.Caused by Procedure Rev Error. Relationship of Suction Point Will Be Verified |
- on 910801,determined That Two Procedures for Documenting Vol of Fuel Stored in DG Fuel Oil Storage Tank Erroneously Revised.Caused by Procedure Rev Error. Relationship of Suction Point Will Be Verified
| 10 CFR 50.73(a)(2)(1) | | 05000302/LER-1992-004, :on 920428,emergency Feedwater Block Valves Failed to Close During Differential Pressure Testing.Caused by Normal Valve Wear & Inadequate Motor Operator Capabilities.Cable Combinations Modified |
- on 920428,emergency Feedwater Block Valves Failed to Close During Differential Pressure Testing.Caused by Normal Valve Wear & Inadequate Motor Operator Capabilities.Cable Combinations Modified
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000302/LER-1992-005, :on 920429,determined That EDG Could Exceed Max Rating for Certain Makeup Pump Operational Lineups. Caused by Failure to Analyze Consequences of Loss of Offsite Power Event.Surveillance Procedures Revised |
- on 920429,determined That EDG Could Exceed Max Rating for Certain Makeup Pump Operational Lineups. Caused by Failure to Analyze Consequences of Loss of Offsite Power Event.Surveillance Procedures Revised
| | | 05000302/LER-1992-006, :on 920501,four safety-related Pipe Supports Did Not Meet Minimum Fs as Specified in NRC IE Bulletin 79-02.Caused by Design Oversight by Ae Firm in 1984.Sys Modified in Compliance W/Bulletin 79-02 |
- on 920501,four safety-related Pipe Supports Did Not Meet Minimum Fs as Specified in NRC IE Bulletin 79-02.Caused by Design Oversight by Ae Firm in 1984.Sys Modified in Compliance W/Bulletin 79-02
| | | 05000302/LER-1992-006-01, Forwards LER 92-006-01,reflecting Change in Corrective Action Implementation Schedule.Only 12 Supports Spread Among Six Different Sys Affected & Factors of Safety Above 2.0 | Forwards LER 92-006-01,reflecting Change in Corrective Action Implementation Schedule.Only 12 Supports Spread Among Six Different Sys Affected & Factors of Safety Above 2.0 | | | 05000302/LER-1992-007, :on 920501,facility Determined That Calculated Input Voltage to Motor Operators on Two Steam Admission Valves May Experience Voltage Lower than Minimun Required. Caused by Initial Plant Design.Mod in Progress |
- on 920501,facility Determined That Calculated Input Voltage to Motor Operators on Two Steam Admission Valves May Experience Voltage Lower than Minimun Required. Caused by Initial Plant Design.Mod in Progress
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000302/LER-1992-008, :on 920507,discovered That Plant Operated Outside 10CFR50,App R Requirements When Plant Aligned Cooling Water for HPI Pump a to Decay Heat Closed Cycle Cooling.Operating Procedure Revised |
- on 920507,discovered That Plant Operated Outside 10CFR50,App R Requirements When Plant Aligned Cooling Water for HPI Pump a to Decay Heat Closed Cycle Cooling.Operating Procedure Revised
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000302/LER-1992-009, :on 920507,determined That Area Immediately Above Pressurizer Experiencing Temps in Excess of Design for Equipment in Area.Caused by Lack of Adequate Insulation. Insulation to Be Repaired Prior to Outage |
- on 920507,determined That Area Immediately Above Pressurizer Experiencing Temps in Excess of Design for Equipment in Area.Caused by Lack of Adequate Insulation. Insulation to Be Repaired Prior to Outage
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000302/LER-1992-010, :on 920604,determined That Inadequate Level of Detail of Initial Plant Design Calculation Causes Operation Outside Design Basis.Control Transformers Replaced W/Larger Control Transformers |
- on 920604,determined That Inadequate Level of Detail of Initial Plant Design Calculation Causes Operation Outside Design Basis.Control Transformers Replaced W/Larger Control Transformers
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000302/LER-1992-011, :on 920605,failure to Install Electrical Isolation Device in Interlock Relay Branch Circuit Results in Potential Loss of Control Power to Containment Isolation Valve.Control Power Will Be Uninterrupted |
- on 920605,failure to Install Electrical Isolation Device in Interlock Relay Branch Circuit Results in Potential Loss of Control Power to Containment Isolation Valve.Control Power Will Be Uninterrupted
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000302/LER-1992-012, :on 920627,valve in RCS Drop Line Closed, Isolating Suction of Operating DHR Pump from RCS & Interrupting Cooling Water Flow to Reactor Core.Caused by Personnel Error.Training Enhanced |
- on 920627,valve in RCS Drop Line Closed, Isolating Suction of Operating DHR Pump from RCS & Interrupting Cooling Water Flow to Reactor Core.Caused by Personnel Error.Training Enhanced
| | | 05000302/LER-1992-013, :on 920612,during post-maint Testing,Isolation Valve Failed to Close on Demand from Main Cr.Caused by Bent Valve Stems Due to Insufficient Matl Strength.Stem Replaced W/Stem Made of Superior Matl |
- on 920612,during post-maint Testing,Isolation Valve Failed to Close on Demand from Main Cr.Caused by Bent Valve Stems Due to Insufficient Matl Strength.Stem Replaced W/Stem Made of Superior Matl
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000302/LER-1992-014, :on 920701,determined That Computer Alarm for Rod Index Limits Not Updated During Cycle 8 to Reflect Changes Due to Fuel Burnup.Caused by Personnel Error. Procedures Revised to Assure Alarm Updated |
- on 920701,determined That Computer Alarm for Rod Index Limits Not Updated During Cycle 8 to Reflect Changes Due to Fuel Burnup.Caused by Personnel Error. Procedures Revised to Assure Alarm Updated
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000302/LER-1992-015, :on 920717,EFIC Sys Actuation Occurred Due to Low OTSG Level.Plant Startup Procedure Will Be Revised to Assure That Both Main Feedwater Pumps Are Capable of Controlling Main Feedwater Flow |
- on 920717,EFIC Sys Actuation Occurred Due to Low OTSG Level.Plant Startup Procedure Will Be Revised to Assure That Both Main Feedwater Pumps Are Capable of Controlling Main Feedwater Flow
| | | 05000302/LER-1992-016, :on 920804,alert Declared When Fire Lasted for More than 10 Minutes Due to Failure in Alarm Circuit in Battery Charger.Caused by High Current.Failed Rectifier Replaced & Related Fuse Circuit Installed |
- on 920804,alert Declared When Fire Lasted for More than 10 Minutes Due to Failure in Alarm Circuit in Battery Charger.Caused by High Current.Failed Rectifier Replaced & Related Fuse Circuit Installed
| 10 CFR 50.73(a)(2)(x) | | 05000302/LER-1992-017, :on 920808,auxiliary Bldg Ventilation Exhaust Partially Lossed Due to Improper Switch Adjustment & Solinod Failure.Warning Plaques Will Be Installed on Ductwork for Listed Air Handling Fans |
- on 920808,auxiliary Bldg Ventilation Exhaust Partially Lossed Due to Improper Switch Adjustment & Solinod Failure.Warning Plaques Will Be Installed on Ductwork for Listed Air Handling Fans
| | | 05000302/LER-1992-018, :on 920731,discovered That Required Testing of Pressurizer Code Safety Valves Had Not Been Completed.Caused by Personnel Error.Pressurizer Code Safeties Will Be Removed & Tested During Upcoming Maintenance Outage |
- on 920731,discovered That Required Testing of Pressurizer Code Safety Valves Had Not Been Completed.Caused by Personnel Error.Pressurizer Code Safeties Will Be Removed & Tested During Upcoming Maintenance Outage
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000302/LER-1992-019, :on 920902,both Chemical Addition Sys Boric Acid Pumps Declared Inoperable Due to Undersized Thermal Overload Elements.Thermal Overload Elements Replaced W/ Elements Sized to Prevent Tripping |
- on 920902,both Chemical Addition Sys Boric Acid Pumps Declared Inoperable Due to Undersized Thermal Overload Elements.Thermal Overload Elements Replaced W/ Elements Sized to Prevent Tripping
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000302/LER-1992-020, :on 920914,determined That Two of Four HPI Valves May Not Function Under Certain Design Basis Conditions.Caused by Insufficently Detailed Instructions. Control Circuits Rewired & Valves Restored |
- on 920914,determined That Two of Four HPI Valves May Not Function Under Certain Design Basis Conditions.Caused by Insufficently Detailed Instructions. Control Circuits Rewired & Valves Restored
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000302/LER-1992-021, :on 921004,discovered That Fluid Level in Reactor Coolant Pump Lubricating Oil Collection Tanks at 14%.Caused by Personnel Error.Plant Mod to Repair Feedwater Leak & Control Cooling Water Temp Underway |
- on 921004,discovered That Fluid Level in Reactor Coolant Pump Lubricating Oil Collection Tanks at 14%.Caused by Personnel Error.Plant Mod to Repair Feedwater Leak & Control Cooling Water Temp Underway
| | | 05000302/LER-1992-022, :on 921015,discovered That RCP Lube Oil Collection Drain Tanks Exhibited Fluid Level of 19%.Caused by Accumulation of Over 65 Gallons of Water in Tanks.Fluid Drained from Lube Oil Collection Drain Tanks |
- on 921015,discovered That RCP Lube Oil Collection Drain Tanks Exhibited Fluid Level of 19%.Caused by Accumulation of Over 65 Gallons of Water in Tanks.Fluid Drained from Lube Oil Collection Drain Tanks
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000302/LER-1992-023, :on 921110,oversight Discovered in Original App R Analysis Results in Operation Outside Design Basis. Analysis Failed to Realize That MUV-31 Could Fail While closed.MUV-31 Scenerio Reanalyzed |
- on 921110,oversight Discovered in Original App R Analysis Results in Operation Outside Design Basis. Analysis Failed to Realize That MUV-31 Could Fail While closed.MUV-31 Scenerio Reanalyzed
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000302/LER-1992-024, :on 921113,discovered That Several Unistrut Structural Pipe Hangers Did Not Meet Design Requirement. Caused by Design Error.Operability Assessments Will Be Performed & Hangers Replaced or Modified |
- on 921113,discovered That Several Unistrut Structural Pipe Hangers Did Not Meet Design Requirement. Caused by Design Error.Operability Assessments Will Be Performed & Hangers Replaced or Modified
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000302/LER-1992-025, :on 921123,discovered That Surveillance Procedure Had Not Been Performed within Required Time Period.Caused by Method in Which Quarterly Surveillance Requirements Are Scheduled.Plan Revised |
- on 921123,discovered That Surveillance Procedure Had Not Been Performed within Required Time Period.Caused by Method in Which Quarterly Surveillance Requirements Are Scheduled.Plan Revised
| | | 05000302/LER-1992-026, :on 921208,replacement of Failed RCS Flow Transmitter Caused Voluntary Entry Into TS 3.0.3.No Corrective Actions Planned |
- on 921208,replacement of Failed RCS Flow Transmitter Caused Voluntary Entry Into TS 3.0.3.No Corrective Actions Planned
| 10 CFR 50.73(a)(2)(1) | | 05000302/LER-1992-027, :on 921229,plant Tripped Due to High RCS Pressure Caused by Inadequate MFW Flow Reduction.Caused by Buildup of Deposits in Pump Control Actuator.Program Implemented to Replace Mfwp Actuators |
- on 921229,plant Tripped Due to High RCS Pressure Caused by Inadequate MFW Flow Reduction.Caused by Buildup of Deposits in Pump Control Actuator.Program Implemented to Replace Mfwp Actuators
| 10 CFR 50.73(a)(2)(iv), System Actuation |
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