ML102160180
| ML102160180 | |
| Person / Time | |
|---|---|
| Site: | Salem |
| Issue date: | 06/30/2010 |
| From: | Pyle M Public Service Enterprise Group |
| To: | Tuccillo K Office of Nuclear Reactor Regulation, State of NJ, Dept of Environmental Protection, Bureau of Nuclear Engineering |
| References | |
| SCH10-078 | |
| Download: ML102160180 (117) | |
Text
PSEG Nuclear LLC P.O. Box 236, Hancock Bridge, NJ 08038-0236 CERTIFIED MAIL 0nSE Nuclear LLC June 2010 SCH10-078 Karen Tuccillo Radiation Protection Programs Bureau of Nuclear Engineering New Jersey Department of Environmental Protection 33 Arctic Parkway Trenton, New Jersey 08625 QUARTERLY REMEDIAL ACTION PROGRESS REPORT, FOURTH QUARTER 2009 PSEG NUCLEAR, LLC, SALEM GENERATING STATION
Dear Ms. Tuccillo:
PSEG Nuclear LLC (PSEG) has prepared this Quarterly Remedial Action Progress Report (RAPR) summarizing groundwater remediation activities performed during 2009 at the PSEG Nuclear, LLC, Salem Generating Station (Station). The Station is located on Artificial Island in Hancock's Bridge, Salem County, New Jersey.
Groundwater remediation activities are being conducted to address tritium detected in shallow groundwater adjacent to and south of the Salem Unit 1 Reactor Containment and Fuel Handling Building (FHB). The. Station site plan is depicted. on Figure 1 and Figure 2 presents a detailed view of the area undergoing active remediation.
The release of tritium contaminated water to the environment was remedied in February 2003 when the Salem Unit 1 telltale drains were cleared and the Spent Fuel Pool (SFP) water that had accumulated behind the liner was drained. Routine maintenance of the spent fuel pool (SFP) telltale drains has prevented a reoccurrence of the standing water condition responsible for the initial release and has precluded further flow restrictions in those drains. The installed seismic gap drains continue to provide a hydraulic gradient into the building and to the waste treatment systems, and away from the environment.
,The Groundwater Recovery System (GRS) continues to control the flow of shallow groundwater in the shallow unconsolidated zone maintaining the plume to the on-site area while removing the remaining tritiated groundwater.
The monitoring program provides data to support the adaptive management program and analyze the efficiency of the program. Plant related gamma-emitting radioisotopes have not been detected and tritium concentrations have generally continued to decline in groundwater samples, indicating that current activities meets the objectives of the program as provided in the RAWP.
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At present, it is estimated that less than 1 Curie of tritium (approximately 0.89 C) remains in the plume where it exists above the NJDEP Ground Water Quality Criteria (NJGWQC). The mass is estimated based upon a number of factors including: the amount of tritium drawn back through the seismic gap by gap draining activities, the actual degree of variability in the tritium concentrations of the groundwater, and the amount of mass held in dead end pore space.
Additionally, the existing monitoring network was designed to monitor a much more extensive plume; therefore the great reductions in plume mass achieved to date has resulted in the present situation where only a few wells indicate concentrations above the NJGWQC.
The following sections present the background of environmental investigation and remedial action at the site, the details and results of activities conducted since the recent submittal of the 3rd Quarter 2009 RAPR, and provide a discussion of upcoming activities projected for the next reporting period.
1 Project Background In April 2004, a Remedial Investigation Report (RIR) was submitted to the New Jersey Department of Environmental Protection Bureau of Nuclear Engineering (NJDEP-BNE) presenting the details and results of a groundwater'investigation conducted following the discovery of tritium in groundwater adjacent to.Salem Unit 1. The results of the remedial investigation indicated that the source of tritium detected in groundwater was the Spent Fuel Pool, the tritium release to the environment had been stopped, and that tritium had not migrated to the property boundary above the New Jersey GWQC.
Based on the results of the remedial investigation a remedial action strategy was developed to hydraulically limit further migration and reduce the concentration of tritium remaining in groundwater adjacent to Salem Unit 1. In April 2004, PSEG initiated a pilot study designed to demonstrate the effectiveness of groundwater extraction for achieving remedial objectives.
The pilot study proved to be effective, and in July 2004, a Remedial Action Work Plan. (RAWP) proposing the operation of a full-scale groundwater extraction system was prepared and submitted to the NJDEP-BNE. The RAWP was approved by the NJDEP-BNE in November 2004 and a full-scale groundwater extraction system was subsequently installed.
In April 2005, weekly draining of the Unit 1 seismic gap was initiated to ensure that the flow of water entering the seismic gap was directed toward the interior of the building for treatment rather than outward toward the environment. Continuous draining of the Unit 1 seismic gap was initiated in February 2007 and the program has been continued to date.
2 Continued Groundwater Monitoring Groundwater monitoring activities continued through this reporting period in accordance with the schedule provided to NJDEP-BNE.
The sampling program is designed to 2
provide the representative data necessary to evaluate plume containment. Monitoring activities include the periodic collection of groundwater samples from the 36 Station monitoring wells.
A summary of monitoring well construction details is presented in Table 1. Results for plume area monitoring well locations are depicted on Figure 2 and results for wells beyond the area of active remediation are shown on Figure 3.
Groundwater samples are initially submitted to Salem Chemistry for analysis for tritium and gamma-emitting radioisotopes. Samples indicating tritium concentrations less than 50,000 picocuries per liter (pCi/L) are sent to Maplewood Testing Services for more refined analysis yielding lower detection limits.
Historical and current analytical data indicate that plant related gamma-emitting radioisotopes have not been detected in groundwater from any monitoring well since monitoring was initiated in 2003.
Historical analytical tritium results for groundwater collected from the Station monitoring wells are presented on Figure 2 and Table 2. Included on Figure 2 are: panel 1) the extent of tritium in groundwater at the completion of the remedial investigation (Baseline Plume); panel 2) the extent of tritium in groundwater one year prior to the reporting period, December 2008; and, panel 3) the extent of tritium in groundwater in December 2009.
Based on a review of Figure 2, it is apparent that the mass of tritium in groundwater has been significantly reduced by the remedial efforts conducted to date.
Details regarding these activities are discussed below.
The analytical results for groundwater samples collected from the monitoring wells were evaluated based on the water-bearing zone in which they are screened.
The three primary water-bearing units investigated beneath the Station are: 1) the Vincentown Formation; 2) the shallow water-bearing unit within the limits of the cofferdam surrounding Salem Unit 1; and, 3) the shallow, water-bearing unit outside the limits of the cofferdam.
2.1 Tritium Analytical Results for the Vincentown Formation The following wells are screened in the Vincentown Formation: Well V, Well K, Well L, Well P, Well Q, and Well CB. Groundwater quality for Well K, Well L, Well P, and Well Q is currently monitored on a semi-annual basis. Groundwater quality for Well V and Well CB is currently monitored on a quarterly and monthly basis, respectively.
Tritium has consistently not been detected above laboratory detection limits or detected at relatively low levels in groundwater at all monitoring wells screened within the Vincentown formation since the initiation of monitoring at these locations with the recent exception of Well CB. As discussed in the Q3, 2009 RAPR concentrations of tritium increased slightly at well CB following the March/April 2008 outage, during which the steam generators in Unit 2 were replaced. The activities involved in the spring 2008 outage resulted in damage to Well CB which is presently in the process of being assessed and repaired.
Tritium levels temporarily increased in Well CB during the 3
summer of 2008 but have been trending toward levels historically observed in other wells completed in the Vincentown formation since approximately spring 2009. At no time did tritium concentrations rise to a level approaching the New Jersey Groundwater Quality Criteria. Thus, the groundwater monitoring results continue to indicate that the previous release of tritium impacted water from the SFP has not significantly migrated below the shallow water-bearing unit.
2.2 Tritium Analytical Results for Wells Installed Within the Limits of the Cofferdam The following wells are screened in the shallow, water-bearing unit within the limits of the cofferdam: Well M, Well N, Well 0, Well R, Well AC, Well AE, Well Al, Well AM, Well AN, and Well AO. Groundwater quality for these wells is currently monitored on a monthly basis.
However, Well AN has been out of service and Well AO was inaccessible for much of the year. These wells have therefore not been sampled.
These wells are scheduled for service in 2010 and samples will be collected from these wells following servicing.
Groundwater collected from Well AD, Well AJ, and Well AM exhibit some of the highest concentrations of tritium remaining at the Site, likely due to their location relative to the original release. Tritium concentrations in groundwater at these wells exhibits general decreasing trends since the initiation of monitoring in 2003. Well AC, for example, the location of the historic highest concentrations, has exhibited steadily decreasing concentrations (from a maximum of 15,000,000 pCi/L in April 2003 to 27,471 pCi/L during the sampling event in December 2009). The decrease in tritium concentrations observed at Well AC provides confirmation that the remedial groundwater recovery system (GRS) is effectively reducing concentrations of previously released tritium and there are no further releases of tritium to the environment.
Tritium concentrations at Well N, Well 0, Well R, Well AE and Well Al are below GWQC and generally show consistent declining temporal trends. Tritium concentrations at all well locations within the cofferdam have generally decreased by one order of magnitude or more since the initiation of monitoring, indicating that remedial activities are effectively removing mass from the areas of greatest concentration.
Variations in concentration occur primarily due to the complex flow patterns and limited flushing within the limits of the cofferdam.
2.3 Tritium Analytical Results for Wells Installed Outside the Limits of the Cofferdam The wells installed in the shallow, water-bearing unit beyond the limits of the cofferdam are Well S, Well T, Well U, Well W, Well Y, Well Z, Well AA, Well AB, Well AD, Well AF, Well AG (Shallow and Deep), Well AH (Shallow and Deep), Well AJ, Well AL, Well AP, Well AQ, Well AR, Well AS, Well AT, and Well CA. These wells are screened either just above the clay confining unit that separates the shallow water-bearing unit from the 4
Vincentown Formation, or in the interval indicating the highest tritium concentrations found in the shallow water-bearing unit at each boring location at the time of the Supplemental Investigation completed in August 2003.
Tritium concentration trends for wells screened in the shallow, water-bearing unit indicate that the operation of the groundwater extraction system is achieving the remedial action objectives (i.e., reduce the mass of tritium in groundwater and maintain hydraulic control).
The distribution of tritium in groundwater in December 2009 is presented on Figure 2, along with the distribution of tritium prior to the initiation of the pilot study in March 2004, and in December 2008. As shown on Figure 2, the mass of tritium in groundwater has continued to decrease through the operation of the groundwater extraction pilot study system and operation of the full-scale GRS.
3 Groundwater Extraction Groundwater extraction as a remedial strategy at the site was initiated with the operation of a pilot test from April 2004 to February 2005.
In accordance with the RAWP, groundwater extraction activities completed to date consisted of the operation of the pilot-study from April 26, 2004 to February 11, 2005 and operation of the full scale GRS from February 16, 2005 to the present. As discussed above, system service was scheduled and performed in October 2008 to address valve and pump difficulties. An additional service event was performed in the spring of 2009 to service pumps that were not performing to their design expectations.
3.1 Full-Scale System The objectives of the full-scale GRS consist of:
" maintaining hydraulic containment of the tritium plume; and
" reducing tritium concentrations in groundwater.
The present operation of the GRS consists of groundwater extraction from Wells AB, AD, AJ, AS, and AT. Pumping at Well S has not occurred since 2006 as a result of low yield and resulting pump failures. A regular system service schedule was implemented beginning in the fourth quarter of 2009 to maximize system operation and efficiency.
Groundwater extracted from the wells is processed in accordance with the Station's United States Nuclear Regulatory Commission (USNRC) license and plant procedures.
Details of the extracted effluent are discussed below.
3.2 Mobile Groundwater Recovery Unit The mobile groundwater recovery unit was designed and built to target specific areas of the groundwater plume exhibiting greater tritium concentrations.
The mobile 6nit typically operates between March and November (weather permitting).
Water is 5
collected in nominal 1,000 gallon batches for handling in accordance with the station's permits. The mobile unit has historically been used successfully at Wells 0, AP, AM, and AR.
In 2009 it was operated at Wells 0 and AR where relatively elevated concentrations were present during the early and latter part of the year, respectively.
3.3 Total System Effluent Data and Evaluation GRS operations were initiated on February 16, 2005. The system operated in various configurations as part of the optimization process for approximately the first month. The GRS discharges continuously in accordance with the Station's USNRC permit allowing the GRS to be more effective and efficient than the pilot-scale system. As of December 2009, the GRS has recovered greater than 24 million gallons of groundwater. This is equivalent to an average recovery rate of approximately 10.8 gallons per minute or greater than 15 times the recharge rate for the extraction area (calculated to be 0.7 gallons per minute, based upon an assumed percentage of annual precipitation).
3.4 Water-Level Data and Evaluation Water level measurements from the extraction and select observation wells have been monitored to confirm hydraulic containment of the tritium groundwater plume. Water levels are periodically collected and evaluated according to the schedule described in the Q4 2006 RAPR submitted in March 2007.
Groundwater elevation contours developed from water level measurements collected in March, May, September and December of 2009 are presented in Figures 4, 5, 6, and 7, respectively. The GRS system was serviced in the spring of 2009. The system continues to control the flow of groundwater in the Salem Unit 1 yard area and therefore controls the distribution of the remnants of the tritium groundwater plume.
3.5 Cumulative Curies Removed The various groundwater recovery activities conducted to date have been successful in controlling the plume and recovering tritium from groundwater at and downgradient of the Salem Unit 1 seismic gap.
Figure 8 summarizes the results of groundwater remediation activities conducted using the well field including both the pilot study and the permanent system. As shown on Figure 8, approximately 3.1 curies1 of tritium have been recovered from the operation of the GRS through December 2009. Approximately 1, curie (0.93 curies) of tritium was removed by the pilot system.
Therefore, a total of 4.1 curies of tritium have been removed by the GRS. As the mass remaining in the plume continues to decrease so will the rate of tritium recovery by the GRS.
The effectiveness of the GRS is emphasized by the decrease and stabilization of system effluent concentrations since the activation of the full scale system in February 2005. System effluent concentrations
'The 3Q09 RAPR indicated approximately 3.25 curies had been removed based on visual interpretation of the graph. The current estimate is based on the calculation modeling performed annually in the fourth quarter.
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averaged 6,323 pCi/L during the fourth quarter 2009. This indicates that the GRS has been successful at significantly decreasing tritium concentrations in groundwater as discharge concentrations are roughly 6 percent of the peak concentration (109,000 pCi/L) observed in March 2005. The average effluent concentration during 2009 was 10,256 pCi/L, indicating that the GRS continues to reduce the mass present in the subsurface of the Salem Unit 1 yard area.
The mass of tritium in the plume was recalculated in late 2008 in order to provide an annual. update of the remedial progress.
This interval has been selected based upon the adaptively managed sampling program such that the most complete data set is used to calculate the mass remaining in the plume. At the end of 2008 the mass was estimated to be less than one curie.
Recalculation of tritium mass as of December 2009 shows tritium concentrations, where they exists above the NJDEP GWQC, are now estimated to be slightly less than 0.9 Curie This calculation is based upon the estimated amount of tritium in each originally defined model layer based upon concentration and pore volume. The endpoint for the mass calculation is the 20,000 pCi/L concentration isocontour. Therefore it is expected that GRS operations will achieve end criteria for tritium, (20,000 pCi/L) removal within two years wihich is ahead of the previously communicated schedule although the system will likely remain in some form as a fail safe for the release mechanism.
4.0 Operation of the Seismic Gap Drain In addition to the operation of the GRS and mobile groundwater recovery unit, the seismic gap drains in Salem Unit 1 and Unit 2 are being used to continuously drain the water from these gaps, resulting in the recovery of tritium concentrations from the seismic gap. The operation of these permanent gap drains creates an inward gradient towards the gaps facilitating the recovery of water from low accessibility areas and minimizing the potential for this water to enter the environment.
Water samples from the seismic gap drains are periodically collected for tritium analysis. Table 3 and Figure 9 summarize the results of periodic tritium analysis from the seismic gap. A comparison of Figure 2 and Figure 9 indicates that concentrations of tritium in water recovered in the Unit 1 seismic gap have been consistently significantly higher than those detected in groundwater samples collected from Well AC and Well AM located to the southeast and southwest of the seismic gap, respectively.
Thus, continuous operation of the Unit 1 seismic gap drain is effectively removing SFP water in the seismic gap, resulting in no release of tritium to groundwater adjacent to the seismic gap. Tritium concentrations in water presently being removed from the gap are close to the concentrations present in the pool indicating that the continuous draining program has been successful in establishing a more direct flow path between the seismic gap drain and any SFP water.
Continuous or nearly continuous draining (resulting in a hydraulic head less than that which is present in the geologic materials present outside the seismic gap) provides positive assurance that the engineering control established by the seismic gap drain is effective at capturing any SFP water that enters the seismic gap. The gap drain creates 7
an inward gradient such that groundwater flows into the seismic gap assuring that no further potential exists for a discharge to the environment from the gap. Concentrations of tritium from the Unit 1 seismic gap (summarized by week) are shown on Figure 9.
Monitoring of water drained from the Unit 2 seismic gap acts as a screen for a potential release from the Unit 2 SFP. Water collected in the Unit 2 seismic gap drain indicate tritium levels several orders of magnitude below the Unit 1 seismic gap drain concentration, and consistent with the trends in the Unit 1 seismic gap drain.
Water samples will continue to be obtained on a weekly basis from the Unit 1 and Unit 2 seismic gap drain to evaluate the potential for the release of radioisotopes to the environment.
Upcoming Activities Activities projected for the first half of 2010 (January through June) include the following:
Continue to monitor continuous draining of seismic gap drains; Ongoing evaluation of the data to refine the procedures and protocols as necessary to adaptively manage the operation and sampling of the GRS; Continue to measure groundwater levels and evaluate flow and plume containment; Perform the spring GRS service event to evaluate and recondition wells S, AB, AJ, AN and AT; Repair/reprogram wells AO and AN; Continued groundwater sampling and analysis; and, Continued operation and evaluation of the GRS performance.
Based on the decreasing trends in most wells, PSEG recommends modifying the minimum sampling frequency of wells, especially those that are routinely below the NJGWQC. Based on the extensive split sampling program conducted to date and the consistency of the data, PSEG also recommends reducing the level of quality assurance provided by BNE by reducing the split sampling program.
It is also recommended that operating wells connected to the GRS system be sampled on a monthly basis to aid in the adaptive management of the GRS system.
If you have any questions or comments regarding the contents of this report, please do not hesitate to contact me at (856) 339-5066.,
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Sincerely, 94ý( D.f-Mark Pyle Manager - Salem Chemistry, Environmental, and Radwaste C
Joe Furia - NRC NRC - Salem Resident Inspector NRC - Document Room 9
BC:
Chris White H15 Edwin Eilola S05 Edward Keating N21 John Valeri Jr.
T5 Christine Neely N21 Helen Gregory N21 File#Groundwater EXTERNAL Peter Milionis, ARCADIS Christopher Sharpe, ARCADIS
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S I of 2 Table 01.
Well Construction Details, PSEG Nuclear, LLC, Salem Generating Station, Hancock's Bridge, New Jersey.
Installation Construction Diameter Total Depth Monitoring Monitored MP MP Northing Easting Well ID Date Details (inches)
(feet bgs)
Interval Hydrogeologic Elevation Elevation (NAD 83)
(NAD 83)
(feet bgs)
Unit (feet RPD)
(feet amsl)
Well K Feb-03 Sch-40 PVC 2
80.0 70.0-80.0 Vincentown1 102.00 12.08 231,435 199,697 Well L Jan-03 Sch-40 PVC 2
80.0 70.0 - 80.0 Vincentown1 101.46 11.54 230,933 199,263 Well M May-03 Sch-40 PVC 1
20.0 10.0 -20.0 Cofferdam2 102.17 12.25 230,843 199,546 Well N Jan-03 Sch-40 PVC 2
20.0 10.0-20.0 Cofferdam2 101.65 11.73 230,777 199,661 Well 0 Jan-03 Sch-40 PVC 2
20.0 10.0-20.0 Cofferdam2 101.33 11.41 230,804 199,839 Well P Mar-03 Sch-40 PVC 2
80.0 70.0-80.0 Vincentown1 101.13 11.21 230,336 200,000 Well Q Mar-03 Sch-40 PVC 2
.80.0 70.0-80.0 Vincentown' 106.59 16.67 230,645 201,196 Well R Jun-03 Sch-40 PVC 1
19.0 9.0- 19.0 Cofferdam2 102.35 12.43 230,906 199,640 Well S4 May-03 Sch-40 PVC 2
34.7 24.7-34.7 Shallow3 99.04 9.12 230,711 199,613 Well T Jun-03 Sch-40 PVC 2
31.2 21.2-31.2 Shallow3 104.13 14.21 231,575 199,575 Well U4 May-03 Sch-40 PVC 2
32.2 27.2-32.2 Shallow3 98.57 8.65 231,370 199,618 Well V4 Jun-03 Sch-40 PVC 2
79.5 69:5 - 79.5 Vincentown' 98.74 8.82 231,355 199,548 Well VV4 Jun-03 Sch-40 PVC 2
35.0 25.0- 35.0 Shallow3 98.26 8.34 230,777 199,450 Well Y Sep-03 S9h-40 PVC 2
37.0 27.0-35.0 Shallow3 101.81 11.89 230,771 199,343 Well Z Sep-03 Sch-40 PVC 2
37.5 27.5-37.5 Shallow3 101.86 11.94 230,681 199,399 Well AA 4 Sep-03 Sch-40 PVC 2
36.0 26.0-36.0 Shallow3 99.07 9.15 230,603 199,541 Well AB 4 Oct-03 Sch-40 PVC 2
42.0 32.0- 42.0 Shallow3 98.93 9.01 230,623-199,677 Well AC 4 Sep-03 Sch-40 PVC 2
24.0 14.0 -24.0 Cofferdam 2 98.77 8.85 230,724 199,725 Well AD 4 Oct-03 Sch-40 PVC 6
43.0 33.0 -43.0 Shallow3 98.99 9.07 230,684 199,607 Well AE Oct-03 Sch-40 PVC 2
37.5 27.5-37.5 Cofferdam 2 101.54 11.62 230,829 199,845 Notes:
MP bgs RPD amsl 2
3 4
Measuring Point Below ground surface Relative to plant datum Relative to mean sea level (NAVD 1988)
Monitoring well is screened in the Vincentown Formation.
Monitoring well is screened in the shallow, water-bearing unit at a location within the limits of the cofferdam.
Monitoring well is screened in the shallow, water-bearing unit at a location outside the limits of the cofferdam.
The surface completions of Monitoring Wells S, U, V, W, AA, AB, AC, and AD were converted from above-grade to flush-grade in February 2004.
S e
Well Construction Details, PSEG Nuclear, LLC, Salem Generating Station, Hancock's Bridge, New Jersey.
2 of 2 Table 01.
Installation Construction Diameter Total Depth Monitoring Monitored MP MP Northing Easting Well ID Date Details (inches)
(feet bgs)
Interval Hydrogeologic Elevation Elevation (NAD 83)
(NAD 83)
(feet bgs)
Unit (feet RPD)
(feet amsl)
45.0 35.0-45.0 Shallow3 101.61 11.69 230,491 199,702 Well AG-Shallow Feb-04 Sch-40 PVC 1
24.2 14.2 - 24.2 Shallow3 99.29 9.37 230,496 199,508 Well AG-Deep Feb-04 Sch-40 PVC 1
40.0 30.0 -40.0 Shallow 3 99.20 9.28 230,496 199,508 Well AH-Shallow Feb-04 Sch-40 PVC 1
24.5 14.5-24.5 Shallow3 102.58 12.66 230,450 199,596 Well AH-Deep Feb-04 Sch-40 PVC 1
40.0 30.0 -40.0 Shallow3 102.70 12.78 230,450 199,596 Well Al Jan-04 Sch-40 PVC 4
22.0 12.0 - 22.0 Cofferdam2 98.79 8.87 230,798 199,521 Well AJ Jan-04 Sch-40 PVC 4
35.3 15.3 - 35.3 Shallow3 98.85 8.93 230,670 199,665 Well AL Jan-04 Sch-40 PVC 2
25.3 15.3-25.3 Shallow3 99.13 9.21 230,594 199,806 Well AM Jan-04 Sch-40 PVC 4
20.9 10.9-20.9 Cofferdam2 98.55 8.63 230,762 199,680 Well AN Jun-04 Sch-40 PVC 4
25.0 10.0-25.0 Cofferdam2 98.76 8.84 230,727 199,735 Well AO Jun-04 Sch-40 PVC 4
21.0 11.0-21.0 Cofferdam2 98.82 8.90 230,765 199,556 Well AP Jun-04 Sch-40 PVC 4
40.0 15.0-40.0 Shallow3 98.65 8.73 230,694 199,464 Well AQ Jun-04 Sch-40 PVC 4
45.0 20.0-45.0 Shallow3 99.05 9.13 230,526 199,540 Well AR Jun-04 Sch-40 PVC 4
43.0 18.0-43.0 Shallow3 99.22 9.30 230,622 199,626 Well AS Jun-04 Sch-40 PVC 4
41.5 16.5-41.5 Shallow3 99.44 9.52 230,566 199,604 Well AT Jun-04 Sch-40 PVC 4
44.0 19.0 -44.0 Shallow3 99.25 9.33 230,546 199,566 Well BW Dec-06 Sch-40 PVC 1
10 5-10 Shallow1 98.72 8.80 231563.00 199,864 Well BX Dec-06 Sch-40 PVC 1
10 5-10 Shallow1 98.72 8.80 231582.00 199,876 Well CA Dec-06 Sch-40 PVC 4
38 28.0 -38.0 Shallow2 98.87 8.95 231318.00 199,791 Well CB Dec-06 Sch-40 PVC 2
80 70.0-80.0 Vincentown3 98.98 9.06 231328.00 199,787 Notes:
MP bgs RPD amsl 1
2 3
4 Measuring Point Below ground surface Relative to plant datum Relative to mean sea level (NAVD 1988)
Monitoring well is screened in the Vincentown Formation.
Monitoring well is screened in the shallow, water-bearing unit at a location within the limits of the cofferdam.
Monitoring well is screened in the shallow, water-bearing unit at a location outside the limits of the cofferdam.
The surface completions of Monitoring Wells S, U, V, W, AA, AB, AC, and AD were converted from above-grade to flush-grade in February 2004.
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium Major Cations and Aniums Identification Date Note lResult (pCi/L) I'LLD IDeviation Boron(nsg/L) ISodium(mg/.ýl)
Well-K Well-K Well-K Well-K Well-K Well-K Well-K Well-K Well-K Well-K Well-K Well-K Well-K Well-K Well-K Well-K Well-K Well-K Well-K Well-K Well-K Well-K Well-K Well-K Well-K Well-K Well-K Well-K Well-K 01/29/03 02/03/03 02/05/03 02/12/03 02/27/03 03/14/03 03/18/03 03/26/03 03/31/03 04/09/03 04/17/03 04/21/03 04/29/03 05/05/03 05/20/03 05/28/03 06/04/03 06/10/03 06/17/03 06/24/03 06/30/03 07/16/03 07/29/03 08/12/03 08/27/03 09/09/03 09/25/03 10/06/03 11/09/03
-153
-153 1,120 506 1,170 937 875 822 677 1,010 1,170 911 833 948 878 859 921 897 894 783 914 870 950 845 852 653 713 880 891 153 153 147 148 145 144 144 140 155 140 141 140 142 135 145 141 141 138 141 141 142 140 140 142 141 147 139 143 141 90 91 104 96 104 100 99 97 103 99 102 98 97 96 100 97 98 97 98 96 99 97 98 98 97 98 94 99 98 0.74 0.8 1.38 1.19 1,060 1,210 1,200 1,060 1,190 1,220 1,170 1,280 1,250 1,330 1.13 1.02 1.16 0.82 1.15 0.92 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
[0000 Constituent was dejected above its New Jersey Groundwater Quality Criteria.
N ot Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page I of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sampl Ii Tritim IMajor Catiosand Anions I
Identification Date Note lSesolt (pCi/L) I LLD IDeviation Boron(mg/L) ISodium(:mg/):
Well-K 02/04/04 762 139 95 Well-K 06/10/04 777 143 97 Well-K 08/02/04 720 144 97 0.67 1,160 Well-K 10/04/04 485 156 100 Well-K 11/03/04 598 148 98 1.60 1,270 Well-K 12/06/04 1
-4,520 4,520 1,370 Well-K 01/10/05 480 152 98 2.12 1,200 Well-K 02/01/05 602 139 93 Well-K 03/03/05 711 146 98 Well-K 04/05/05 740 143 97 Well-K 05/09/05 473 155 100 Well-K 07/05/05 721 150 101 Well-K 01/09/06 511 155 100 Well-K 07/10/06 404 153 97 Well-K 01/23/07 468 152 98 Well-K 07/12/07 294 144 90 Well-K 01/16/08 358 138 88 Well-K 07/16/08 200 129 80 Well-K 01/19/09 186 145 89 Well-K 07/16/09 295 141 89 Well-L 01/22/03
-147 147 87 0.76 1,020 Well-L 01/23/03
-146 146 86 0.67 1,890 Well-L 01/24/03
'147 147 87 0.59 2,000 Well-L 01/27/03
-151 151 89 0.53 1,900 Well-L 03/14/03
-143 143 85 Well-L 03/18/03
-143 143 86 Well-L 04/02/03
'153 153 91 Well-L 04/08/03
-142 142 86 Notes:
LLD mg/L Lower Limit of Detection Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
F Constituent was detected above its New Jersey Groundwater Quality Criteria.
'Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 2 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium I
Major Cations and Anions Identification Date INote ýResýult (pCi/L) I LLD Deviation IBoron(mg/L) ISodium(mg/L)
Well-L Well-L Well-L Well-L Well-L Well-L Well-L Well-L Well-L Well-L Well-L Well-L Well-L Well-L Well-L Well-L Well-L Well-L Well-L Well-L Well-L Well-L Well-L Well-L Well-L Well-L Well-L Well-L Well-L 04/15/03 04/24/03 04/29/03 05/05/03 05/15/03 05/20/03 05/28/03 06/04/03 06/10/03 06/17/03 06/24/03 06/30/03 07/29/03 08/27/03 09/25/03 12/16/03 03/23/04 05/04/04 05/10/04 05/19/04 05/24/04 06/10/04 07/07/04 08/02/04 10/04/04 11/03/04 12/06/04 01/10/05 02/01/05
-141
-139
-141
-134
' 144
-144
-141
-140
-137
-141
'141
-140
-141
-142
-140
-146 3,870
'138
'138
'148
-147 140 753
-147
'159
-142
'4,520
-158
-148 141 139 141 134 144 144 141 140 137 141 141 140 141 142 140 146 147 138 138 148 147 140 140 147 159 142 4,520 158 148 84 82 83 82 85 86 84 84 82 84 84 83 86 84 84 86 137 82 84 88 88 85 96 88 92 84 1,280 93 87 1.95 1.62 2,330 2,490 2,180 1,140 1.56 0.81 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
[
onstituent was detected above its New Jersey.Groundwater Quality Criteria.
NNot Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 3 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L)
Sodinm(mg/L)
Well-L 03/07/05
'158 158 94 0.832 2,400 Well-L 04/06/05
'152 152 90 Well-L 05/17/05
,150 150 88 Well-L 07/06/05
-152 152 90 Well-L 01/09/06
-160 160 95 Well-L 07/10/06
,156 156 92 Well-L 01/22/07
-154 154 92 Well-L 07/19/07
-145 145 87 Well-L 01/17/08
-137 137 81 Well-L 07/16/08
'129 129 78 Well-M 02/12/03 18,700 170 270 0.25 23 Well-M 02/28/03 14,400 146 219 0.17 28 Well-M 03/03/03 9,420 140 181 0.16 27 Well-M 03/10/03 15,000 144 223 0.21 22 Well-M 03/17/03 10,600 142 192 Well-M 03/24/03 10,100 144 189 Well-M 03/31/03 11,000 154 203 Well-M 04/07/03 9,260 136 181 Well-M 04/14/03 9,600 135 183 Well-M 04/21/03 8,880 140 180 Well-M 04/30/03 8,800 143 180 Well-M 07/09/03 12.,0001 138 602 Well-M 07/23/03 113*00*1, 141 573 Well-M 08/06/03 73,200 144 462 0.24 22 Well-M 08/06/03 ZM21LI 141 466 Well-M 08/20/03
'20 141 430 0.27 23 Well-M 09/04/03 39,700 K
143 346 0.22 23 Well-M 09/16/03
ýLý 33,00 141 320 0.32 25 Notes:
LLD mg/L pCi/L Lower Limit of Detection Milligrams per liter Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
Fijoo Constituent was detected above its New Jersey Groundwater Quality Criteria.
-qA"Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 4 of 93 0
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium Major Cationsmand)Anionm Idetfto DI t Not Result (pCi/L)j LLD IDeviation IBoron(mg/L)SdimngL Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M 10/03/03 10/20/03 10/30/03 12/04/03 01/06/04 01/22/04 02/17/04 03/05/04 04/29/04 05/11/04 06/10/04 07/08/04 08/17/04 09/08/04 10/04/04 11/03/04 12/06/04 01/19/05 01/19/05 02/09/05 03/02/05 04/11/05 05/03/05 06/06/05 07/12/05 08/15/05 09/06/05 10/10/05 11/14/05 16,380 11,200 8,900 7,340 11,300 7,170 6,510 2,350 3,610 5,090 3,857 3,745 3,036 2,818
-4,520 10,031 15,169 17,049 12,528 146 NA NA 146 145 140 NA 146 141 141 141 144 143 146 144 143 4,520 2,650 3,950 4,660 3,360 4,220 147 146 3,750 3,905 4,940 148 158 289 NA NA 198 183 164 NA 168 159 117 133 150 136 137 126 125 1,390 2,830 2,890 3,240 3,400 2,550 192 225 4,070 4,114 4,037 240 219 0.27 25 0.15 0.12 22 21 3.33 24 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
Fi"ioT Constituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 5 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample ITritiums major Cations and Aniona Identification Date Note Result (pCi/L) I LLD I
Deviation Boron(mg/L)
Sodium(mgIL)
Well-M 12/13/05 8,257 148 178 Well-M 01/17/06 6,932 152 170 Well-M 02/21/06 7,371 153 174 Well-M 02/22/06 1
7,510 3,550 1,750 Well-M 03/20/06 1
4,200 3,730 1,530 Well-M 04/11/06 4,067 155 144 Well-M 05/16/06 4,592 152 148 Well-M 06/19/06 4,712 155 150 Well-M 07/18/06 5,553 157 161 Well-M 08/08/06 4,912 161 157 Well-M 09/18/06 4,132 161 148 Well-M 10/10/06 3,565 157 139 Well-M 11/01/06 4,077 170 154 Well-M 12/18/06 3,887 162 147 Well-M 01/13/07 4,517 150 148 Well-M 02/23/07 4,796 168 161 Well-M 03/08/07 5,085 158 160 Well-M 04/20/07 11,617 170 225 Well-M 05/15/07 10,479 181 219 Well-M 06/18/07 8,426 147 177 Well-M 07/18/07 7,443 146 168 Well-M 08/15/07 6,066 140 154 Well-M 09/20/07 5,271 150 153 Well-M 10/03/07 5,612 160 164 Well-M 11/14/07 4,505 124 133 Well-M 12/12/07 4,617 151 146 Well-M 01/17/08 4,713 140 141 Well-M 02/06/08 4,733 139 141 Well-M 03/18/08 4,946 145 147 Notes:
LLD mg/L pCi/L Lower Limit of Detection Milligrams per liter Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
,00C onstituent was detected above its New Jersey Groundwater Quality Criteria.
N
'Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 6 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritiumo Major Cations and Anions Identification Date Note Rlesnlt (pCiI) I"LLD Deviation IBoron(mgf]L) ISodiuinmg/j Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M Well-M 04/02/08 05/08/08 06/19/08 07/07/08 08/06/08 09/02/08 11/19/08 12/15/08 01/08/09 01/27/09 02/11/09 02/18/09 02/25/09 03/05/09 03/10/09 03/19/09 03/26/09 03/30/09 04/08/09 04/16/09 04/22/09 04/29/09 05/11/09 05/26/09 06/08/09 09/02/09 10/08/09 11/17/09 12/16/09 4,755 4,893 4,969 4,980 4,755 4,523 4,000 4,347 46.230 343,026 41,8151\\
142 147 135 129 140 134 135 149 145 150 151 146 145 147 145 3,210 142 145 146 134 134 134 143 3,530 3,920 147 140 145 146 142 146 140 137 140 135 131 142 365 362 358 343 316 312 310 4,170 291 319 330 302 299 279 319 3,860 5,090 421 307 317 301 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
.00o) Constituent was detected above its New Jersey Groundwater Quality Criteria.
IANot Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 7 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample I
Tritium Major Cations and Anios Identification Date Note Result (pCiIL)I LLD I
Deviation Boron(mg/L)
Sodium(mg/L)
Well-N 01/30/03 58,400 141 412 0.37 14 Well-N 01/30/03 69,OUO 187 505 0.34 14 Well-N 02/10/03 15,600 149 229 0.28 11 Well-N 03/04/03 2,770 144 123 0.2 34 Well-N 03/14/03 2,670 143 121 0.41 24 Well-N 03/17/03 3,830 142 134 0.36 21 Well-N 03/25/03 3,480 139 129 Well-N 04/04/03 3,560 152 137 Well-N 04/11/03 3,730 137 131 Well-N 04/16/03 3,910 142 134 Well-N 04/25/03 4,600 138 140 Well-N 04/30/03 9,370 144 185 Well-N 05/06/03 9,830 137 186 Well-N 05/21/03 7,480 144 169 Well-N 05/27/03 7,130 141 165 Well-N 06/04/03 5,480 141 150 Well-N 06/11/03 4,990 137 144 Well-N 06/19/03 5,680 142 153 Well-N 06/25/03 5,060 142 146 Well-N 07/10/03 5,020 137 144 Well-N 07/25/03 5,220 141 148 Well-N 08/07/03 5,110 145 148 0.21 24 Well-N 08/20/03 5,850 140 153 0.25 20 Well-N 09/04/03 5,660 145 154 0.33 23 Well-N 09/17/03 6,160 141 157 0.27 22 Well-N 10/03/03 5,740 145 157 0.24 24 Well-N 10/03/03 1
6,460 NA NA Well-N 11/03/03 1
5,560 NA NA Notes:
LLD mg/L pCi/L Lower Limit of Detection Milligrams per liter Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
[
p(C onstituent was detected above its New Jersey Groundwater Quality Criteria.
qA Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 8 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium IaMajor Cations and Anions Identification I
Dma tel Note lResult (pCiIL) 1 L15D Deviation IBoron(nig/L) ISodium(mg/L)
Well-N Well-N Well-N Well-N Well-N Well-N Well-N Well-N Well-N Well-N Well-N Well-N Well-N Well-N Well-N Well-N Well-N Well-N Well-N Well-N Well-N Well-N Well-N Well-N Well-N Well-N Well-N Well-N Well-N 12/12/03 01/20/04 02/11/04 02/11/04 03/18/04 04/08/04 05/12/04 06/03/04 07/20/04 08/17/04 09/14/04 10/25/04 11/23/04 12/27/04 01/12/05 02/22/05 03/15/05 04/19/05 05/17/05 06/21/05 07/12/05 08/15/05 09/20/05 10/10/05 11/14/05 12/20/05 01/23/06 02/23/06 03/21/06
,6,010 6,050 5,950 7,360 6,550 7,180 8,210 9,890 5,220 14,303 11,642 10,619 9,150 7,660 9,550 9,442 9,712 9,781 9,060 9,302 8,147 8,152 7,502 8,280 8,210 5,896 7,400 8,410 13,500 NA 143 139 NA 145 137 147 152 141 161 148 157 149 4,060 154 146 153 147 147 145 147 157 151 149 151 157 149 3,920 3,730 NA 155 154 NA 162 164 178 196 148 235 207 206 187 1,720 195 186 195 193 185 183 177 184 174 180 180 162 171 1,810 2,130 2.30E-01 17 0.11 18 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
Constituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 9 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L)
Sodium(mg/L)
Well-N 04/11/06 8,393 164 189 Well-N 05/16/06 8,588 152 185 Well-N 06/20/06 15,289 150 232 Well-N 07/18/06 6,660 159 170 Well-N 08/21/06 13,776 154 224 Well-N 09/07/06 22,714 155 277 Well-N 09/19/06 14,486 160 232 Well-N 10/09/06 2&U37K>
159 310 Well-N 11/01/06 11,023 165 213 Well-N 11/15/06 10,407 197 232 Well-N 12/07/06 9,280 211 233 Well-N 12/18/06 10,163 154 199 Well-N 01/13/07 6,325 148 165 Well-N 01/22/07 6,812 157 173 Well-N 02/06/07 11,587 189 234 Well-N 02/23/07 12,517 167 227 Well-N 03/08/07 13,252 146 218 Well-N 04/20/07 6,332 160 172 Well-N 05/15/07 8,139 150 177 Well-N 06/19/07 7,554 145 169 Well-N 07/18/07 8,865 99 168 Well-N 08/15/07 9,045 148 182 Well-N 09/21/07 9,711 147 188 Well-N 10/03/07 2iL30 145 267 Well-N 10/17/07 22,16 153 279 Well-N 11/14/07 18,607 124 237 Well-N 12/12/07 12,763 145 207 Well-N 01/17/08 8,049 139 170 Well-N 01/28/08 7,780 139 167 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
gw dConstituent was detected above its New Jersey Groundwater Quality Criteria.
NANot Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 10 of 93 0
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 well Sample Trtium Major Cations and An i
Identification Date Note Result (pCi/L) I LLD I
Deviation Boron(mg/L) I Sodium(mg/L)
Well-N 02/06/08 7,641 148 172 Well-N 02/20/08' 6,853 138 160 Well-N 03/13/08 6,278 149 161 Well-N 03/18/08 6,956 137 160 Well-N 04/02/08 7,427 150 171 Well-N 04/23/08 7,017 143 163 Well-N 05/08/08 6,949 139 159 Well-N 06/24/08 8,406 135 168 Well-N 07/07/08 9,346 144 183 Well-N 08/07/08 9,026 142 178 Well-N 08/21/08 9,675 129 176 Well-N 09/02/08 9,899 128 178 Well-N 11/14/08 8,991 142 177 Well-N 12/08/08 8,845 133 172 Well-N 01/08/09 9,873 133 179 Well-N 02/25/09 8,830 148 180 Well-N 03/26/09 10,761 133 185 Well-N 04/16/09 7,695 138 165 Well-N 05/20/09 9,024 145 179 Well-N 06/10/09 L iU*
133 298 Well-N 07/21/09 10,848 132 186 Well-N 08/18/09 11,347 138 191 Well-N 09/23/09 10,342 148 191 Well-N 10/20/09 10,276 139 186 Well-N 11/17/09 10,133 146 188 Well-N 12/16/09 10,016 154 193 S
Well-o 101/29/03 1 11 400 1 43 1 106 0.17 1
40 Well-O 01/29/03
'1,220 156 110 0.16 41 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
onstituent was detected above its New Jersey Groundwater Quality Criteria.
N0Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page I11 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample ITritium I
aor Cations and Anions Identification Date Note Result (pCiL)I LLD I Deviation.
Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 02/10/03 02/21/03 02/28/03 03/04/03 03/13/03 03/17/03 03/25/03 03/31/03 04/07/03 04/15/03 04/21/03 04/29/03 05/06/03 05/21/03 05/28/03 06/03/03 06/10/03 06/17/03 06/24/03 07/09/03 07/25/03 08/06/03 08/20/03 09/03/03 09/15/03 10/03/03 10/20/03 11/17/03 12/18/03 10,300 7,370 11,700 8,800 12,300 11,000 8,660 8,010 7,290 12,400 11,800 10,500 10,200 11,100 12,700 12,200 12,800 10,300 13,400 9,100 7,710 8,300 7,440 6,400 7,730 6,980 6,700 5,320 149 149 147 142 143 155 141 155 137 141 139 140 134 143 140 140 137 141 141 139 139 148 142 143 141 145 141 NA 145 193 170 201 178 204 206 178 180 165 204 201 191 187 197 207 202 206 190 212 182 169 178 168 159 170 168 161 NA 150 0.1 0.09 0.09 0.07 0.11 0.08 13 15 17 21 16 12 0.24 0.31 0.28 0.27 0.23 0.2 14 14 14 13 23 47 I
Notes:
LLD mg/L Lower Limit of Detection Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
fao 6()Constituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 12 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Wen Sample Tritium Major Cations and Anions Identification Date Note IResult (pCi/L) I LLD
[
Deviation Boron(mg/L) I Sodium(mg/L)
Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 01/14/04 02/09/04 02/09/04 03/03/04 03/23/04 04/06/04 05/03/04 05/11/04 06/10/04 06/24/04 07/13/04 07/29/04 08/31/04 09/22/04 10/04/04 10/18/04 11/22/04 12/16/04 01/18/05 02/08/05 03/08/05 04/11/05 05/10/05 06/07/05 07/06/05 07/19/05 08/02/05 09/07/05 10/04/05 3,750 19,300 14,174 9,510 6,739 7,307 6,637 5,543 5,874 14,027 15,000 18,840
~25,4O01 10,911 7,096 6,722 5,803 3,827 4,999 4,295 5,400 4,326 141 NA NA NA NA 136 140 140 4,974 141 141 146 159 146 140 150 144 3,230 152 4,660 139 148 148 147 145 156 148 146 153 132 NA NA NA NA 247 253 254 2,855 218 185 163 179 167 151 161 218 1,950 257 2,640 195 170 166 156 136 154 143 152 146 2.81E-01 0.297 120 f
22 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
Constituent was detected above its New Jersey Groundwater Quality Criteria.
5&kot Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 13 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium I
Major Cations and Anions Identification I
Date INote IResult (pCi/L) I LLD IDeviation I oron(nsg/L) ISodium(mg/L)
Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0
-Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 11/02/05 12/09/05 01/16/06 02/07/06 03/07/06 04/04/06 05/02/06 06/19/06 07/17/06 08/21/06 09/18/06 10/05/06 11/02/06 12/07/06 01/13/07 02/24/07 03/07/07 04/20/07 05/16/07 06/18/07 07/19/07 08/15/07 09/19/07 10/04/07 11/19/07 12/12/07 01/16/08 02/07/08 03/12/08 I
14,530 15,734 18,595 8,560 7,340 9,369 9,417 9,533 4,760 4,237 12,747 19,760 9,060 r45;398 15,782 15,749 8,610 9,155 1,525 2,619 6,211 i37L.51A 151 152 3,550 157 3,310 161 152 155 151 152 158 157 169 162 147 153 155 163 180 148 145 142 146 183 149 142 144 149 149 224 235 2,460 254 1,720 178 191 194 188 150 147 219 275 197 306 292 393 393 257 229 177 178 109 146 167 340 291 317 340 Notes:
LLD mg/L pCi/L Lower Limit of Detection Milligrams per liter Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
2o
]Constituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 14 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 well Sample Tritium Major Cations and Anions Identification I
Date INote FResulIt (pCi/L)
LLD Deviation Boron(mg/L) jSodiuns(ng/L)
Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 04/01/08 05/19/08 05/27/08 06/11/08 06/23/08 07/15/08 07/28/08 08/18/08 08/25/08 09/02/08 10/17/08 11/18/08 12/16/08 01/09/09 01/27/09 02/24/09 03/16/09 04/01/09 05/13/09 05/26/09 06/03/09 06/15/09 07/21/09 07/29/09 08/18/09 08/25/09 09/23/09 10/20/09 11/04/09 13,799 10,565 10,568 9,377 9,388 12,170
-4,530 9,760 9,780 10,128 50.098 18,107 17,479 17,711 10,671 13,279 10,124 12,355 14,474 15,862 16,153 148 146 150 146 135 128 143 4,530 4,280 134 135 135 152 4,530 140 149 3,210 5,160 145 146 135 131 134 140 140 139 150 138 147 289 215 195 192 175 173 203 NA 1,930 178 184 285 333 4,170 379 372 5,390 5,070 266 240 231 229 186 206 185 200 221 222 228 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
Fj,-oooIConstituent was detected above its New Jersey Groundwater Quality Criteria.
NT Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 15 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample ITritium Major Cations and Anions Identification Date Note Result (pCi/L) I LLD I
Deviation Boron(mg/L)
Sodium(mg/L)
Well- 0 12/22/09 14,064 140 210-I Well-P 02/05/03 0.18 1,600 Well-P 02/06/03
'153 153 91 Well-P 02/21/03
'148 148 91 Well-P 03/13/03 303 143 90 0.2 Well-P 03/18/03 465 143 92 Well-P 03/26/03
-143 143 87 Well-P 04/03/03
-154 154 9
Well-P 04/24/03
-139 139 82 Well-P 04/29/03
,144 144 85 Well-P 05/05/03
'134 134 82 Well-P 05/20/03
'145 145 85 Well-P 05/30/03
'142 142 85 Well-P 06/04/03
'141 141 84 Well-P 06/10/03
-138 138 84 Well-P 06/17/03
-141 141 85 Well-P 06/24/03
-141 141 85 Well-P 07/16/03
'141 141 85 Well-P 08/13/03
-140 140 84 0.48 1,570 Well-P 09/08/03
-147 147 87 0.65 1,560 Well-P 09/09/03 1
-7,430 7,430 NA Well-P 10/06/03
'143 143 86 0.48 1,610 Well-P 01/22/04
-144 144 86 Well-P 04/28/04
'139 139 83 0.441 1,550 Well-P 08/03/04
' 157 157 92 0.292 1,540 Well-P 10/05/04
'149 149 87 Well-P 11/03/04
'147 147 87 0.955 1,690 Well-P 12/14/04 1
'3,230 3,230 1,010 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
20,000' Constituent was detected above its New Jersey Groundwater Quality Criteria.
NANot Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 16 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium r Cations and Anis Identification Date Note Result (pCiIL)
SodiumnS(mg/L)
Well-P 01/11/05
-162 162 95 1.02 1,580 Well-P 02/09/05
-148 148 88 Well-P 03/03/05
-158 158 92 Well-P 04/12/05
-149 149 89 Well-P 05/10/05
-148 148 87 Well-P 07/11/05
-151 151 89 Well-P 01/23/06
-150 150 89 Well-P 07/24/06
-155 155 93 Well-P 01/14/07
-154 154 92 Well-P 07/19/07
-146 146 86 Well-P 01/24/08
'137 137 81 Well-P 07/16/08
'144 144 86 Well-P 01/27/09
'150 150 88 Well-P 07/22/09
-142 142 85 Well-Q 02/06/03
'147 147 88 Well-Q 03/11/03
-142 142 85 Well-Q 03/12/03
'141 141 84 Well-Q 03/14/03
-143 143 85 Well-Q 03/19/03
'143 143 85 Well-Q 03/24/03
'143 143 85 Well-Q 04/23/03
'139 139 82 Well-Q 04/30/03
'142 142 84 Well-Q 05/06/03
-135 135 81 Well-Q 05/12/03
'144 144 84 Well-Q 05/19/03
-144 144 84 Well-Q 05/30/03
-140 140 84 Well-Q 06/05/03
'139 139 83 Well-Q 06/11/03
'138 138 83 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
F Constituent was detected above its New Jersey Groundwater Quality Criteria.
Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 17 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) I LLD I
Deviation Boron(mg/L)
Sodium(mg/L)
Well-Q 06/16/03
-141 141 84 Well-Q 06/23/03
-143 143 85 Well-Q 07/17/03
-141 141 85 Well-Q 08/13/03
-142 142 85 0.32 1,830 Well-Q 09/10/03
-148 148 89 0.25 1,790 Well-Q 10/07/03
-144 144 85 0.33 1,920 Well-Q 11/09/03
-142 142 86 0.32 1,930 Well-Q 01/08/04
'142 142 83 0.3 1,850 Well-Q 02/04/04
'139 139 84 Well-Q 03/22/04
'144 144 85 0.285 1,720 Well-Q 06/04/04
-156 156 91 Well-Q 08/02/04
-146 146 88 0.28 1,630 Well-Q 10/04/04
'153 153 87 Well-Q 11/03/04
-150 150 88 0.312 1,960 Well-Q 12/29/04 1
-4,020 4,020 1,420 Well-Q 01/31/05 213 142 89 Well-Q 02/15/05 1
-3,910 3,910 1,130 Well-Q 03/14/05
' 151 151 91 0.30 1,730 Well-Q 03/15/05 151 151 91 1,730 Well-Q 04/18/05
-145 145 85 Well-Q 05/16/05
-151 151 88 Well-Q 07/19/05
'150 150 89 Well-Q 01/23/06
-150 150 90 Well-Q 07/10/06
'159 159 93 Well-Q 01/08/07
'157 157 92 Well-Q 07/24/07
-146 146 86 Well-Q 01/28/08
'137 137 81 Well-Q 07/24/08
'139 139 83 Well-Q 01/27/09
-146 146 86 Notes:
LLD mg/L pCi/L Lower Limit of Detection Milligrams per liter Picocuries per liter 1
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
20 0o00 Constituent was detected above its New Jersey Groundwater Quality Criteria.
Ný Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 18 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCiIL)
Sodium(mg/L)
Well-Q 07/29/09 1
142 142 83 I
I Well-R 02/26/03 13,900 145 218 0.29 43 Well-R 03/03/03 7,490 140 166 0.23 37 Well-R 03/10/03 6,170 145 158 0.27 29 Well-R 03/17/03 7,270 144 168 0.27 33 Well-R 03/25/03 6,810 140 162 Well-R 04/01/03 6,740 153 169 Well-R 04/08/03 5,940 135 152 Well-R 04/14/03 5,890 142 154 Well-R 04/22/03 5,800 139 153 Well-R 04/30/03 5,260 141 148 Well-R 07/09/03 3,270 136 125 Well-R 07/25/03 2,940 141 124 Well-R 08/06/03 2,860 144 124 0.46 54 Well-R 08/20/03 2,860 142 124 0.51 48 Well-R 09/04/03 2,990 153 132 0.57 46 Well-R 09/17/03 2,800 141 122 0.47 50 Well-R 10/03/03 2,740 146 125 0.4 52 Well-R 10/21/03 2,650 140 120 Well-R 12/05/03 2,550 147 122 0.37 50 Well-R 01/22/04 2,210 143 116 Well-R 02/09/04 2,230 140 115 Well-R 02/09/04 1
-5,390 5,390 NA Well-R 03/05/04 2,200 146 117 Well-R 04/28/04 1
-5,780 5,780 1,649 0.265 42 Well-R 05/24/04 2,420 144 120 0.30 41 Well-R 06/10/04 2,390 148 123 0.24 42 Well-R 07/08/04 2,050 147 118 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
F Constituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 19 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample ITritium Major Cations and Anions Identification Date Note Result (pCiIL)
Sodium(mg/L)
Well-R 08/17/04 2,124 159 126 Well-R 09/29/04 2,000 156 122 Well-R 10/11/04 1,708 143 110 Well-R 11/08/04 1,696 151 115 Well-R 12/27/04 1
-4,053 4,053 1,290 Well-R 01/19/05 2,420 159 129 Well-R 02/09/05 2,450 150 123 0.122 45 Well-R 03/15/05 2,704 147 125 Well-R 04/11/05 2,742 157 132 Well-R 05/03/05 2,755 151 128 Well-R 06/22/05 2,736 151 127 Well-R 07/20/05 2,486 147 122 Well-R 08/16/05 2,752 155 130 Well-R 09/20/05 2,673 159 131 Well-R 10/10/05 2,435 149 123 Well-R 11/14/05 2,149 148 119 Well-R 12/13/05 1
-4,370 4,370 NA Well-R 01/17/06 2,131 151 120 Well-R 02/21/06 2,262 153 122 Well-R 03/20/06 1
4,350 3,730 1,560 Well-R 04/11/06 2,192 160 125 Well-R 05/16/06 2,010 150 118 Well-R 06/19/06 2,067 160 124 Well-R 07/18/06 2,090 156 123 Well-R 08/08/06 1,940 148 116 Well-R 09/18/06 2,138 162 126 Well-R 10/10/06 1,943 157 121 Well-R 11/15/06 2,395 164 132 Well-R 12/18/06 3,092 154 134 Notes:
LLD mg/L Lower Limit of Detection Milligrams per liter pCi/L Picocuries per liter 1
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
[
o Constituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 20 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium Major Cations and Anions Identification I
Date Note Rgesult (pCiIL)I LLD Deviation Boron(mg/L) ISodium(mg/L)
Well-R Well-R Well-R Well-R Well-R Well-R Well-R Well-R Well-R Well-R Well-R Well-R Well-R Well-R Well-R Well-R Well-R Well-R Well-R Well-R Well-R Well-R Well-R Well-R Well-R Well-R Well-R Well-R Well-R 01/13/07 02/23/07 03/08/07 04/20/07 05/15/07 06/18/07 07/18/07 08/15/07 09/20/07 10/03/07 11/14/07 12/12/07 01/17/08 02/06/08 03/18/08 04/02/08 05/08/08 06/19/08 07/07/08 08/06/08 09/02/08 11/19/08 12/15/08 01/08/09 02/11/09 03/05/09 04/08/09 05/11/09 06/08/09 3,208 3,563 3,487 3,180 2,567 2,844 2,862 3,000 3,104 2,799 3,029 2,951 2,892 2,941 3,159 3,294 3,173 3,196 3,077 3,158 3,075 2,998 3,075 2,986 3,100 5,052 3,037 3,423 3,596 154 167 161 157 138 142 145 143 144 149 141 145 140 150 150 154 155 135 140 142 134 149 150 145 135 145 144 143 131 135 146 143 138 118 122 124 125 127 129 124 125 122 128 131 134 133 122 124 126 120 128 129 125 122 146 125 128 124 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
2oo0o
]Constituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 21 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample ITuitium Major Cations and Anions Identification Date Note Result (pCi/L) I LLD I
Deviation Boron(mgfL)
Sodium(mg/L)
Well-R 09/02/09 3,454 148 132 Well-R 10/08/09 3,291 138 125 Well-R 11/17/09 3,419 145 129 Well-R 12/16/09 3,877 150 137 Well-S 07/09/03 3,S30,004 134 3,120 Well-S 08/07/03 1
2,20.000 NA NA Well-S 08/21/03 1
2,570.000 NA NA Well-S 09/03/03 1
2,30000 NA NA Well-S 09/15/03 1
2,340,000 NA NA Well-S 10/04/03 1
2,180,000 NA NA Well-S 10/13/03 1
2,030,000 NA NA Well-S 10/20/03 1
f2060,000 NA NA Well-S 10/20/03 1
2,030,00 NA NA Well-S 11/09/03 1
1,960,000 NA NA Well-S 11/09/03 1
2.,040.000 NA NA-Well-S 11/09/03 1
1,790*00*
NA NA Well-S 11/26/03 1
2,660,000 NA NA Well-S 01/20/04 1
1,420A0O0 NA NA Well-S 02/17/04 1
1.,250000 NA NA Well-S 03/1 8/04 1
1,220,000 NA NA Well-S 04/06/04 1
1,160....
4,706 15,206 Well-S 05/04/04 1
1i00.,000 5,589 15,212 44.5 35 Well-S 05/19/04 1
fy889.0 5,780 13,380 Well-S 06/25/04 1
120,000 5,270 14,500 Well-S 07/13/04 1
955j)00 3,620 13,800 Well-S 08/09/04 1
S56.000 4,850 13,000 45 Well-S 09/13/04 1
845.000 4,560 13,000 Well-S 11/08/04 1
820,000 3,230 12,800 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
Foo Constituent was detected above its New Jersey Groundwater Quality Criteria.
1NA Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 22 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium F
Ma1jor Cations and Anions-Identification Date Note Result (pCi/L)
Sodium(mg/L)
Well-S 12/28/04 1
661,0041 4,060 11,300 Well-S 01/11/05 1
753000 3,910 12,100 Well-S 02/15/05 1
724,000 3,910 11,900 Well-S 03/07/05 1
36,00 3,490 8,570 Well-S 03/14/05 1
175,000 4,320 6,110 Well-S 03/23/05 1
JN2jO 3,790 6,190 Well-S 03/28/05 1
40,500 6,280 3,540 Well-S 04/18/05 1
326000 4,420 8,380 Well-S 10/17/05 1
90.200 3,790 4,570 Well-S 11/15/05 1
64,700 3,430 3,840 Well-S 12/12/05 64904 155 446 Well-S 04/29/09 41
- '<4:
148 351 Well-T 07/10/03
'147 147 88 Well-T 07/15/03
,140 140 82 Well-T 07/30/03
,141 141 86 Well-T 08/12/03
'140 140 83 0.64 931 Well-T 08/28/03
,141 141 83 0.66 896 Well-T 09/09/03
-147 147 88 0.63 899 Well-T 09/25/03
-142 142 84 0.63 912 Well-T 10/06/03
-146 146 86 0.65 966 Well-T 12/12/03
-149 149 88 Well-T 03/22/04
'142 142 84 0.649 986 Well-T 04/12/04
-141 141 84 0.762 920 Well-T 07/07/04 148 148 87 Well-T 08/02/04
-152 152 91 0.622 894 Well-T 08/31/04
-147 147 87 Well-T 09/22/04
-146 146 87 Well-T 10/11/04
-155 155 91 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
f2oojConstituent was detected above its New Jersey Groundwater Quality Criteria.
-VN ot Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 23 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium major Cations and Anions Identification Date Note Result (pCi/L)
Sodium(mg/L)
Well-T 11/09/04
-148 148 87 Well-T 12/21/04 1
'3,910 3,910 1,340 Well-T 01/10/05
-165 165 96 Well-T 02/01/05 137 135 83 0.638 945 Well-T 03/03/05
,152 152 90 Well-T 04/05/05
-148 148 90 Well-T 05/09/05
-144 144 86 Well-T 07/05/05
-145 145 86 Well-T 10/03/05
-149 149 90 Well-T 01/09/06
-154 154 90 Well-T 04/03/06
-162 162 96 Well-T 07/10/06
-161 161 95 Well-T 10/05/06
-161 161 95 Well-T 10/06/06 1
-6,270 6,270 NA Well-T 01/23/07 193 152 94 Well-T 04/11/07
'168 168 101 Well-T 07/12/07
'147 147 86 Well-T 10/09/07
'152 152 91 Well-T 01/16/08
'141 141 85 Well-T 04/22/08
-145 145 85 Well-T 07/16/08
-130 130 77 Well-T 10/21/08
-146 146 86 Well-T 01/19/09 266 149 93 Well-T 04/01/09 1
'3,830 3,830 NA Well-T 06/10/09
-133 133 80 Well-T 07/16/09
'143 143 87 Well-T 10/20/09
'-139 139 83 Well-U 1 07/10/03 1 1 136 1
136 1 83 I
I Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
Fiiio Constituent was detected above its New Jersey Groundwater Quality Criteria.
NXNot Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 24 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) I LLD Deviation Boron(mg/L) I Sodium(mg/L)
Well-U Well-U Well-U Well-U Well-U Well-U Well-U Well-U Well-U Well-U Well-U Well-U Well-U Well-U Well-U Well-U Well-U Well-U Well-U Well-U Well-U Well-U Well-U Well-U Well-U Well-U Well-U Well-U Well-U 07/16/03 07/29/03 08/12/03 08/27/03 09/09/03 09/25/03 10/06/03 12/12/03 03/22/04 04/12/04 07/07/04 08/02/04 08/31/04 09/22/04 10/04/04 11/03/04 12/06/04 01/10/05 02/08/05 03/03/05 04/05/05 05/09/05 07/05/05 10/03/05 01/09/06 04/03/06 04/06/06 07/10/06 10/05/06 146
-141
-139
-143 148
-139 203
-148
-144 182 162
,152
,148 167
'146 165
-4,520
-157
'149
-147
-142
-148
'143 284
-157
-154
'5,000
'157
-160 NA 141 139 143 147 139 145 148 144 136 150 152 148 152 146 148 4,520 157 149 147 142 148 143 150 157 154 5,000 157 160 86 96 84 87 90 83 90 86 88 84 92 91 90 93 87 91 1,160 93 91 88 86 90 87 94 94 93 NA 95 98 0.34 0.35 0.38 0.34 0.35 0.38 0.392 0.346 0.377 139 144 139 155 140 168 146 143 I
156 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
2 Constituent was detected above its New Jersey Groundwater Quality Criteria.
Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 25 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Identification Date Note lResult (pCi/) I LLD D eviation Boron(mg/L)
Sodium(mg/L)
Well-U 10/06/06 1
-6,270 6,270 NA Well-U 01/22/07 163 152 93 Well-U 04/11/07
,167 167 102 Well-U 07/12/07
-150 150 91 Well-U 10/09/07
,153 153 92 Well-U 01/16/08
-138 138 84 Well-U 05/28/08
,148 148 90 Well-U 07/16/08 189 128 79 Well-U 10/20/08
,145 145 88 Well-U 01/19/09
-154 154 92 Well-U 04/01/09 1
'3,830 3,830 NA Well-U 06/29/09 282 137 86 Well-U 07/16/09 183 143 88 Well-U 10/20/09 172 140 86 Well-V 07/21/03 334 140 89 Well-V 07/29/03 285 142 89 Well-V 08/12/03 278 142 89 0.5 568 Well-V 08/27/03 338 141 90 0.61 584 Well-V 09/09/03 337 150 95 0.57 582 Well-V 09/25/03
.261 140 87 0.47 670 Well-V 10/06/03 185 144 89 0.46 543 Well-V 11/19/03 1
-3,300 3,300 NA Well-V 12/12/03 207 147 91 Well-V 03/22/04 290 144 90 0.46 556 Well-V 04/12/04 316 137 87 0.529 567 Well-V 07/07/04 228 145 90 Well-V 08/02/04 309 154 97 0.433 504 Well-V 08/31/04 395 151 96 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
[i2 o Constituent was detected above its New Jersey Groundwater Quality Criteria.
XNot Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 26 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium Major Cations and Aniona Identification Date Note Result (pCi/L)
LLD I
Deviation Boron(mg/L) I Sodium(mg/L)
Well-V 09/22/04 402 141 91 Well-V 10/04/04 340 146 92 Well-V 11/03/04 224 143 89 Well-V 12/06/04 1
-4,170 4,170 1,360 Well-V 01/10/05 394 151 96 Well-V 02/08/05 307 152 95 Well-V 03/03/05 157 156 95 0.436 431 Well-V 04/05/05 294 141 89 Well-V 05/09/05 244 155 96 Well-V 07/05/05 197 144 89 Well-V 10/03/05 346 147 93 Well-V 01/09/06 264 157 98 Well-V 04/03/06
-152 152 93 Well-V 07/10/06 181 157 96 Well-V 10/05/06
-159 159 95 Well-V 01/22/07 199 157 97 Well-V 04/11/07 154 149 92 Well-V 07/12/07 163 153 94 Well-V 10/09/07 170 153 94 Well-V 01/16/08 176 139 86 Well-V 05/28/08 186 147 90 Well-V 07/16/08 164 130 80 Well-V 10/20/08 195 145 89 Well-V 01/19/09 244 150 93 Well-V 04/01/09 586 134 89 Well-V 07/16/09 198 145 89 Well-V 10/20/09 173 140 86 I
Well-W 07/07/03 10,500 135 189 I
Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762.
Constituent was detected above the laboratory method detection limit.
20,000 Constituent was detected above its New Jersey Groundwater Quality Criteria.
Cot Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 27 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample I
Tritium Major Cations and Anions Identification Date Note Result (pCi/L)I LLD Deviation Boron(mg/L)
Sodinm(mg/L)
Well-W 07/21/03 11,100 140 196 Well-W 08/06/03 11,500 141 200 0.46 211 Well-W 08/07/03 1
6,010 NA NA Well-W 08/19/03 10,700 142 194 0.59 215 Well-W 09/03/03 10,500 143 192 0.53 222 Well-W 09/15/03 10,900 140 195 0.57 237 Well-W 10/03/03 11,100 147 202 0.46 240 Well-W 10/21/03 10,600 147 195 Well-W 11/17/03 1
12,200 NA NA Well-W 11/19/03 1
13,200 NA NA Well-W 12/16/03 15,200 147 226 Well-W 12/16/03 1
15,500 NA NA Well-W 01/14/04 17,100 144 232 Well-W 02/02/04 19,600 144 251 Well-W 03/03/04 5,320 146 151 0.28 273 Well-W 04/29/04 4,570 140 140 0.14 212 Well-W 05/10/04-2,350 141 117 Well-W 05/24/04 4,080 146 139 Well-W 06/24/04 5,300 141 149 Well-W 07/28/04 11,691 154 208 Well-W 08/02/04 11,910 148 204 Well-W 08/31/04 11,091 160 211 Well-W 09/22/04 9,571 138 186 Well-W 10/11/04 9,947 147 194 Well-W 11/08/04 8,920 150 186 0.487 309 Well-W 12/14/04 1
5,560 3,230 1,390 Well-W 01/10/05 6,292 150 165 0.681 273 Well-W 02/01/05 7,340 159 178 Well-W 03/02/05 5,756 150 158 3.33 27 Notes:
LLD mg/L pCi/L Lower Limit of Detection Milligrams per liter Picocuries per liter 1
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
odý Constituent was detected above its New Jersey Groundwater Quality Criteria.
Nq Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 28 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCiIL) I LLD I
Deviation Boron(mg/L) I Sodium(mg/L)
Well-W Well-W Well-W Well-W Well-W Well-W Well-W Well-W Well-W Well-W Well-W Well-W Well-W Well-W Well-W Well-W Well-W Well-W Well-W Well-W Well-W Well-W Well-W Well-W Well-W Well-W Well-W Well-W Well-W 04/05/05 05/02/05 06/06/05 07/06/05 08/01/05 09/06/05 10/03/05 11/14/05 12/20/05 01/17/06 02/07/06 02/21/06 03/07/06 03/20/06 04/03/06 04/17/06 05/02/06 05/15/06 06/06/06 06/19/06 07/10/06 07/24/06 08/07/06 08/21/06 09/07/06 09/18/06 10/09/06 10/24/06 11/01/06 8,826 12,339 11,480 16,672 14,920 17,419 12,455
,23.40 4>6.200 56.200f 36,755 1,234 3,471 5,284 12,991 15,311 18,859 9,929 12,968 155 147 154 149 149 154 149 3,430 3,430 3,550 3,090 3,920 3,310 3,730 5,000 5,510 5,000 5,000 155 4,890 161 152 158 162 158 166 166 155 170 192 209 207 239 227 247 211 2,460 2,830 3,380 3,470 3,620 3,750 3,850 3,880 4,240 3,800 3,870 374 3,500 144 109 139 162 220 242 266 194 231 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
I--,ooo Constituent was detected above its New Jersey Groundwater Quality Criteria.
7-Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 29 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L)
Sodium(mg/L)
Well-W 11/15/06 14,464 171 245 Well-W 12/07/06 10,046 184 220 Well-W 12/19/06 15,062 139 221 Well-W 01/13/07 18,705 152 259 Well-W 02/05/07 Z4,113 147 278 Well-W 03/08/07 5,838 165 169 Well-W 04/20/07 1,616 159 120 Well-W 06/18/07 1,530 142 107 Well-W 07/18/07 2,462 147 121 Well-W 08/15/07 3,000 147 127 Well-W 09/20/07 6,562 149 164 Well-W 10/03/07 12,492 165 229 Well-W 11/14/07 13,071 123 202 Well-W 12/12/07 13,940 147 216 Well-W 01/17/08 10,203 140 186 Well-W 02/06/08 6,988 141 162 Well-W 03/18/08 2,507 137 116 Well-W 04/02/08 4,169 157 145 Well-W 05/08/08 4,545 146 142 Well-W 06/19/08 5,909 135 149 Well-W 07/07/08 6,880 127 153 Well-W 08/06/08 1,966 132 106 Well-W 09/02/08 2,535 134 114 Well-W 11/18/08 2,919 133 118 Well-W 12/15/08 2,996 139 123 Well-W 01/08/09 4,153 139 135 Well-W 02/11/09 4,498 148 143 Well-W 03/10/09 4,766 144 142 Well-W 04/08/09 4,343 142 139 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
[ijoo Constituent was detected above its New Jersey Groundwater Quality Criteria.
Nq ot Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 30 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample ITritiums Major Cations and Anin Identification Date Note Result (pCiIL) I LLD I
Deviation Boron(mg/L)
Sodium(mg/L)
Well-W 05/11/09 2,328 136 113 Well-W 06/08/09 2,377 126 107 Well-W 07/21/09 4,728 133 137 Well-W 08/18/09 844 145 99 Well-W 09/02/09 912 147 101 Well-W 10/08/09 4,518 140 138 Weil-W 11/17/09 6,351 149 160 Well-W 12/29/09 5,128 147 148 Well-X 08/20/03 1
-4,820 4,820 NA Well-X 07/20/05 1,500 NA NA Well-Y 10/27/03
-142 142 85 Well-Y 11/09/03
-143 143 85 Well-Y 11/19/03 1
-3,750 3,750 NA Well-Y 11/25/03
-141 141 85 0.82 1,070 Well-Y 12/12/03
-148 148 87 Well-Y 12/22/03
-147 147 87 Well-Y 01/06/04 142 142 85 Well-Y 02/02/04 145 145 84 Well-Y 02/02/04 1
5,390 5,390 NA Well-Y 03/23/04 145 145 86 Well-Y 04/07/04
'136 136 82 0.83 1,080 Well-Y 05/10/04 143 143 85 Well-Y 06/24/04 141 141 86 0.82 1,060 Well-Y 07/28/04
-156 156 90 Well-Y 08/02/04
-157 157 94 Well-Y 08/31/04
-145 145 87 Well-Y 09/08/04
-158 158 94 Well-Y 10/11/04 162 162 96 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
[joop Constituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 31 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample ItTritium I
Major Cations and Anions Identification Date INote lResult (pCiIL) ILLD IDeviation IBoron(mg/L) ISodium(mg/L)
Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y 11/08/04 12/13/04 01/10/05 02/01/05 03/07/05 04/06/05 05/25/05 06/07/05 07/20/05 08/01/05 09/07/05 10/04/05 11/01/05 12/13/05 01/17/06 02/07/06 03/07/06 04/04/06 05/02/06 05/16/06 06/06/06 06/19/06 07/11/06 07/24/06 08/07/06 08/22/06 09/07/06 09/19/06 10/09/06
-151
-3,230
-162
-154
<149
-144
-155
-155
'159
-149
<149
-151
'155
'151
-157
-161
-158
'173
<156
'152
-159
-165
'160
'155
'155
-157
-157
'161
'171 151 3,230 162 154 149 144 155 155 159 149 149 151 155 151 157 161 158 173 156 152 159 165 160 155 155 157 157 161 171 88 1,150 94 92 89 84 92 92 93 89 89 91 93 91 94 94 93 101 91 90 93 97 96 92 93 96 94 95 102 0.801 0.761 1,160 1,190 1,230 1,270 1,290 Notes:
LLD mg/L pCi/L Lower Limit of Detection Milligrams per liter Picocuries per liter 1
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
[iooo Constituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 32 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Wen Sample Tritium Major Cations and Anions Identification Date Note IResult (pCi/L)I LLD I
Deviation Boron(mg/L) I Sodium(mg/L)
Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y Well-Y 10/24/06 11/01/06 11/15/06 12/07/06 12/18/06 01/14/07 02/20/07 03/14/07 04/19/07 05/16/07 06/19/07 07/12/07 08/16/07 09/20/07 10/04/07 11/20/07 12/20/07 03/13/08 04/22/08 05/15/08 06/24/08 07/17/08 08/19/08 09/03/08 10/18/08 11/21/08 12/23/08 01/20/09 02/25/09
'171
'166
'166
'193
-157
-155
'165
'162
'163
-180
-149
-155
-146
-146
-154
'149
'140
-138
'146
-148
-147
'138
-134
-134
-133
-131
-132
-136
-132 171 166 166 193 157 155 165 162 163 180 149 155 146 146 154 149 140 138 146 148 147 138 134 134 133 131 132 136 132 100 100 98 109 92 93 97 94 97 101 87 91 87 88 91 90 82 82 86 87 87 83 79 79 80 78 78 80 79 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
onstituent was detected above its New Jersey Groundwater Quality Criteria.
90Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 33 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) I LLD I
Deviation Boron(mg/L)
Sodium(mg/L)
Well-Y 03/30/09 2,259 133 110 Well-Y 04/27/09
-145 145 87 Well-Y 05/20/09
,133 133 79 Well-Y 05/25/09 1
'3,920 3,920 NA Well-Y 06/10/09
-133 133 79 Well-Y 07/22/09
'141 141 85 Well-Y 08/18/09
-145 145 86 Well-Y 09/24/09
'148 148 87 Well-Y 10/27/09
,135 135 79 Well-Y 11/19/09
'131 131 78 Well-Y 12/30/09
-146 146 85 Well-Z 10/27/03 573 142 94 Well-Z 11/09/03
-140 140 92 Well-Z 11/19/03 1
'3,500 3,500 NA Well-Z 11/24/03 583 141 93 0.5 519 Well-Z 12/12/03 621 141 94 Well-Z 12/22/03 659 140 94 Well-Z 01/06/04 648 142 95 Well-Z 02/02/04 538 145 95 Well-Z 03/23/04 412 144 92 Well-Z 04/07/04 580 137 91 0.5 531 Well-Z 05/10/04 561 142 93 Well-Z 06/24/04 474 147 95 0.51 510 Well-Z 07/28/04 519 150 97 Well-Z 07/29/04 519 150 97 Well-Z 08/02/04 706 159 106 Well-Z 08/31/04 585 152 100 Well-Z 09/08/04 444 141 91 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
[ý
]Constituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
Page 34 of 93 02/24/2010 11:26 AM
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 well Sample I
Tritium-1 1
-Major Cationdiun Identification IDate INote lResult (pCi/L) ILLD Deviation IBoron(mg/L)
SoInmgL Well-Z Well-Z Well-Z Well-Z Well-Z Well-Z Well-Z Well-Z Well-Z Well-Z Well-Z Well-Z Well-Z Well-Z Well-Z Well-Z Well-Z Well-Z Well-Z Well-Z Well-Z Well-Z Well-Z Well-Z Well-Z Well-Z Well-Z Well-Z Well-Z 10/11/04 11/08/04 12/13/04 01/10/05 02/01/05 03/07/05 04/06/05 05/25/05 06/07/05 07/20/05 08/01/05 08/16/05 08/29/05 09/07/05 09/19/05 10/04/05 10/18/05 11/01/05 12/13/05 01/17/06 02/07/06 02/21/06 03/07/06 03/20/06 04/04/06 04/17/06 05/02/06 05/16/06 06/06/06 268 339
-3,230 249 228 192 274
-149 182 177 202
-160 186 201
-156 271
-153
-158
-157
-153 240 238
-3,310
-3,730
-177
-160
-153
-151
-163 144 155 3,230 159 153 153 165 149 149 158 147 160 149 149 156 148 153 158 157 153 149 152 3,310 3,730 177 160 153 151 163 90 98 1,060 99 95 94 103 91 91 97 91 98 91 92 94 93 93 94 96 93 93 94 NA NA 108 96 93 93 99 0.491 0.535 0.506 548 688 716 635 702 696 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
F-u-Constituent was detected above its New Jersey Groundwater Quality Criteria.
- N
-Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 35 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium major Cations and Anions Identification Date Note Result (pCiIL)
Sodium(mg/L)
Well-Z 06/19/06
-155 155 94 Well-Z 07/11/06 194 159 98 Well-Z 07/24/06 211 151 93 Well-Z 08/07/06
-157 157 96 Well-Z 08/22/06 217 161 99 Well-Z 09/07/06
-160 160 97 Well-Z 09/19/06
-163 163 99 Well-Z 10/09/06
-160 160 95 Well-Z 10/24/06
-160 160 97 Well-Z 11/01/06
-162 162 97 Well-Z 11/15/06 248 155 96 Well-Z 12/07/06
-203 203 120 Well-Z 12/18/06
-175 175 107 Well-Z 01/14/07
-155 155 94 Well-Z 02/20/07
-152 152 91 Well-Z 03/14/07
-164 164 98 Well-Z 04/19/07 217 160 99 Well-Z 05/16/07
-143 143 85 Well-Z 06/19/07 154 148 90 Well-Z 07/12/07
-150 150 90 Well-Z 08/16/07
-146 146 88 Well-Z 09/20/07 156 145 89 Well-Z 10/04/07 173 153 94 Well-Z 11/20/07
-147 147 90 Well-Z 12/20/07
-138 138 83 Well-Z 03/13/08
-137 137 84 Well-Z 04/22/08
-143 143 86 Well-Z 05/15/08
-148 148 89 Well-Z 06/24/08 136 136 83 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
TConstituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 36 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Weil sample Tritium Major Cations and Anions Identification Date Note IResult (pCi/L)
LLD -
Deviation Boron(mg/L)
Sodium(mg/L)
Well-Z 07/17/08 138 138 84 Well-Z 08/19/08 173 134 83 Well-Z 09/03/08 195 134 83 Well-Z 10/18/08 278 132 83 Well-Z 11/21/08 289 132 83 Well-Z 12/23/08 253 133 83 Well-Z 01/20/09 277 134 84 Well-Z 02/25/09 244 137 86 Well-Z 03/30/09 1,043 133 95 Well-Z 04/27/09 225 142 88 Well-Z 05/20/09 288 135 85 Well-Z 06/10/09 250 133 83 Well-Z 07/22/09 398 144 92 Well-Z 08/18/09 300 143 90 Well-Z 09/24/09 315 148 93 Well-Z 10/27/09 369 142 90 Well-Z 11/19/09 368 149 94 Well-i 12/30/09 210 146 90 Well-AA 10/27/03 613 141 93 Well-AA 11/10/03 645 141 94 Well-AA 11/19/03 1
3,750 NA NA Well-AA 11/24/03 639 145 96 0.25 253 Well-AA 12/10/03 785 141 96 WelU-AA 12/22/03 682 142 95 Well-AA 01/06/04 713 141 95 Well-AA 02/09/04 1,130 139 100 Well-AA 02/19/04 1
-5,390 5,390 NA Well-AA 03/18/04 2,610
- 140, 120 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
Oo7 Constituent was detected above its New Jersey Groundwater Quality Criteria.
Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 37 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample ITritium Major Cations and Anions Identification Date Note Result (pCi/L) I LLD I
Deviation Boron(mgIL)
Sodium(mg/L)
Well-AA 04/12/04 3,140 140 126 2.40E-01 169 Well-AA 05/03/04 1
-5,590 5,590 1,770 Well-AA 05/19/04 1
-3,320 3,320 1,198
<3.3 168 Well-AA 06/23/04 4,376 142 141
<3.33 138 Well-AA 07/29/04 1,650 156 118 Well-AA 08/02/04 1,580 148 112 Well-AA 08/31/04 1,543 159 118 Well-AA 09/08/04 1,512 152 113 Well-AA 10/11/04 1,529 146 110 Well-AA 11/08/04 1,927 152 118 0.59 147 Well-AA 12/14/04 1
-3,230 3,230 1,130 Well-AA 01/11/05 6,640 151 168 Well-AA 02/02/05 11,100 154 205 Well-AA 02/02/05 11,150 155 205 Well-AA 03/07/05
's 1
142 260 0.036 152 Well-AA 04/06/05 1
3-700) 0 4220 2,970 Well-AA 05/02/05 1
22,300 3,320 2,310 Well-AA 06/06/05 16,136 150 235 Well-AA 07/06/05 14,547 150 226 Well-AA 08/01/05 13,174 155 220 Well-AA 09/06/05 15,887 150 234 Well-AA 09/07/05 1
13,500 4,940 2,271 Well-AA 10/03/05 10,930 148 199 Well-AA 11/01/05 8,911 159 189 Well-AA 12/08/05 5,255 147 151 Well-AA 01/10/06 6,416 159 168 Well-AA 02/06/06 5,683 182 177 Well-AA 03/06/06 4,251 157 146 Well-AA 04/04/06 3,483 158 140 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
M e(oConstituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
S 02/24/2010 11:26 AM Page 38 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sampl e Tritium I
Major Cations and Anions Identification Date Note lResult (pCi/L) I'LLD IDeviation IBoron(mg/L) ISodiummgL WelI-AA Well-AA WelI-AA Well-AA Well-AA Well-AA Well-AA WelI-AA Well-AA WelI-AA WelI-AA WelI-AA WeI1-AA WelI-AA WelI-AA Well-AA Well-AA Well-AA WelI-AA WelI-AA Well-AA WelI-AA WelI-AA WelI-AA WelI-AA Well-AA Well-AA Well-AA Well-AA 05/01/06 06/06/06 07/17/06 08/08/06 09/06/06 10/09/06 11/02/06 12/08/06 01/13/07 02/05/07 03/07/07 04/19/07 05/15/07 06/18/07 07/13/07 08/15/07 09/19/07 10/03/07 11/14/07 12/12/07 01/23/08 02/21/08 03/12/08 04/01/08 05/08/08 06/19/08 07/07/08 08/07/08 09/02/08 3,625 2,813 2,745 2,647 2,651 2,302 2,413 1,847 2,236 1,518 1,871 1,805 1,422 1,336 1,569 1,423 1,238 1,460 1,166 1,521 1,570 1,414 1,569 1,536 1,474 1,498 1,423 1,459 1,475 149 168 162 157 158 158 167 179 161 147 155 158 167 144 148 144 150 161 141 137 142 140 138 151 146 146 138 131 134 137 138 133 129 130 126 133 134 128 110 120 121 120 105 110 106 107 119 103 104 107 104 105 112 108 108 103 99 101 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
[Tijooo Constituent was detected above its New Jersey Groundwater Quality Criteria.
Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 39 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Wen Sample ITritium Major Cations and Anions Identification Date Note Result (pCi/L)
Sodium(mg/L)
Well-AA 10/17/08 1,360 135 100 Well-AA 11/18/08 1,381 131 98 Well-AA 12/15/08 1,456 135 101 Well-AA 01/08/09 1,615 133 102 Well-AA 02/24/09 1,605 140 107 Well-AA 03/16/09 1,885 133 106 Well-AA 04/08/09 1,722 141 109 Well-AA 05/11/09 1,479 138 103 Well-AA 06/03/09 1,512 133 101 Well-AA 07/21/09 1,520 142 107 Well-AA 08/04/09 1,406 144 106 Well-AA 09/02/09 1,481 135 102 Well-AA 10/08/09 1,428 139 103 Well-AA 11/04/09 1,419 131 99 Well-AA 12/29/09 1,336 144 105 Well-AB 10/28/03 1
292.000 NA NA Well-AB 11/02/03 1
280,000 NA*
NA Well-AB 11/19/03 1
321.000 NA NA Well-AB 12/04/03 1
409,001 NA NA Well-AR 12/16/03 1
396000 NA NA Well-AB 12/16/03 1
489,000 NA NA Well-AB 01/14/04 1
281,000 NA NA Well-AB 02/17/04 1
215,000 NA NA Well-AB 03/03/04 1
193.001.
NA NA Well-AB 04/06/04 1
2 4,70.6 7,380 Well-AB 05/04/04 1
,136,001 5,589 5,817 9.3 134 Well-AB 05/11/04 1
144,00) 5,392 5,967 Well-AB 05/19/04 1
172,000 5,780 6,108
<3.3 292 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
,oo]Constituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 40 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritiun I
Major Cations and Anions Identification Date INote lResuilt (pCiIL) I LLD Dev7iation IBoron(mg/L) ISodium(mg/L)
Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB 05/24/04 06/03/04 1
1 06/17/04 1 1 07/07/04 07/12/04 07/19/04 07/28/04 08/02/04 08/09/04 08/16/04 08/25/04 09/01/04 09/08/04 09/13/04 09/22/04 10/04/04 10/12/04 10/18/04 11/03/04 11/08/04 11/15/04 11/29/04 12/13/04 01/11/05 01/27/05 01/31/05 02/01/05 02/08/05 03/02/05 213,00 2i10,000
'1A94,000 202,000 1064, 0 0 0K 213,000 1~84,000 164,000~
171,000 >
189,000<
165,000 152,000 1542,00'0~
142,000,
'156,000 4,563 4,563 5,666 3,360 3,620 2,870 4,280 4,420 4,850 3,320 3,030 4,520 3,790 4,560 5,230 3,320 2,220 3,230 2,720 3,230 3,910 2,650 3,230 3,910 2,470 4,560 2,650 4,660 144 6,779 6,746 6,509 6,330 6,380 6,160 6,600 6,120 5,840 5,490 5,880 6,220 5,750 5,980 5,910 6,000 5,520 5,340 5,850 5,650 5,800 5,730 5,410 5,330 5,650 5,770 5,630 5,560 664
<3.3 105 8.12 156 214 15.90 212 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
2 Constituent was detected above its New Jersey Groundwater Quality Criteria.
Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 41 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Wenl Sample Tritium Major Cations and Anions Idetfto Dat Not Result (pCi/L) ILLD Deviation Boron(nsg/L) ISodium(nsgfL)I Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB 03/07/05 03/14/05 03/23/05 03/28/05 04/18/05 05/18/05 06/22/05 08/15/05 10/17/05 11/15/05 12/12/05 01/24/06 02/23/06 03/21/06 04/17/06 05/15/06 06/20/06 07/24/06 09/21/06 01/23/07 02/06/07 06/19/07 08/23/07 09/20/07 10/17/07 10/07/08 04/29/09 05/11/09 06/10/09 1i63,000 153,000 135,000 224,000 97,300 49.S00~<
43,101) 40.81 5,0 14 4186 26UL9$
1,294 6,533 MLV 3,490 4,320 3,790 6,280 4,420 3,490 3,750 3,905 3,790 3,430 4,370 3,550 3,920 3,730 5,510 5,000 4,890 5,470 7,550 159 172 145 141 148 151 150 151 144 141 5,770 5,760 5,830 5,920 5,470 7,050 4,460 3,950 3,730 3,740 3,600 3,480 3,200 3,580 3,990 3,590 3,680 3,540 3,700 158 387 316 283 283 286 108 164 276 327 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
F2o~ooo Constituent was detected above its New Jersey Groundwater Quality Criteria.
Iq--Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 42 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium DT o
Major CationsadAiun/
Identification Date INote [Result (pCi/L) ILLD Deviation IBoron(nsg/L) ISodinns(mg/L)I Well-AC Well-AC Well-AC Well-AC Well-AC Well-AC Well-AC Well-AC Well-AC Well-AC Well-AC Well-AC Well-AC Well-AC Well-AC Well-AC Well-AC Well-AC Well-AC Well-AC Well-AC' Well-AC Well-AC Well-AC Well-AC Well-AC Well-AC Well-AC 10/28/03 11/03/03 11/03/03 11/18/03 11/18/03 12/18/03 01/20/04 02/18/04 03/18/04 04/08/04 06/04/04 07/07/04 07/28/04 08/02/04 08/09/04 08/16/04 08/25/04 09/01/04 01/11/05 01/17/05 02/09/05 04/29/05 05/24/05 06/16/05 07/29/05 08/18/05 09/26/05 11/21/05 I
10.900.000 1~4,2O0,001 14.24000 210,70.000 4,170,000 6.360,0011 6850,000<
3,4.00,0011 394 200,00
~2,230,000 12,040,00 6299.000 614,J000_
NA NA NA NA NA NA NA NA 5,822 6,283 3,360 4,280 3,320 4,850 3,320 3,030 4,520 3,910 3,360 4,660 3,320 3,320 3,750 3,320 4,753 4,220 4,370 NA NA NA NA NA NA NA NA 36,309 26,713 23,200 25,100 23,400 20,900 20,400 19,900 19,400 11,600 11,600 11,200 2,650 2,760 2,520 2,340 6,877 3,390 2,520 253 332 332 31 30
<3.3 17.90 12 71 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
ji.ioo ]Constituent was detected above its New Jersey Groundwater Quality Criteria.
NX Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 43 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium Ma-jor Cations and Anions Identification Date Note Result (pCi/L) I LLD Deviation Boron(mg/L)
Sodium(mg/L)
Well-AC 12/12/05 1
40 4,370 3,340 Well-AC 01/12/06 1
20 3,550 2,770 Well-AC 02/28/06 16,730 153 239 Well-AC 03/23/06 1
5,000 3,360 Well-AC 06/16/06 13,932 158 226 Well-AC 07/14/06 9,709 152 192 Well-AC 08/23/06 1
11:.000 5,100 5,340 Well-AC 09/27/06 13,686 159 224 Well-AC 11/17/06 25,401 143 284 Well-AC 12/28/06 1
31.5oo 3,730 3,010 Well-AC 01/22/07 21,717 159 280 Well-AC 02/12/07 3,1 151 319 Well-AC 03/27/07 20,137 151 265 Well-AC 04/23/07 25,99 0 169 316 Well-AC 05/10/07 20,809 178 287 Well-AC 06/19/07 f22,914 147 268 Well-AC 07/30/07
[ 26 067
?
149 286 Well-AC 08/28/07 31.152 144 308 Well-AC 10/30/07 40.N98 158 370 Well-AC 11/27/07 L 31,460 123 300 Well-AC 12/29/07 1
53,i-0 4,780 4,010 Well-AC 03/30/08 1
5t 0 4,540 3,780 Well-AC 04/29/08 1
7330 4,190 4,400 Well-AC 05/30/08 28,5S4 140 289 Well-AC 06/18/08 M.fk 135 272 Well-AC 07/21/08 2
139 277 Well-AC 08/21/08
- 241,75 128 264 Well-AC 09/22/08 23,562 145 267-Well-AC 10/30/08 23,497 144 268 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
Fi20i-Constituent was detected above its New Jersey Groundwater Quality Criteria.
IN 'N ot Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 44of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 well Sample ITritium Major Cations and Anion Identification Date Note Result (pCi/L) I LLD Deviation Boron(mg/L)
Sodium(mg/L)
Well-AC 11/25/08 244 f9 133 266 Well-AC 12/15/08 26934 152 294 Well-AC 01/23/09 28,061 137 286 Well-AC 02/11/09 26,723 147 289 Well-AC 03/20/09 20,112 126 235 Well-AC 04/27/09 1
27.200 4,290 2,880 Well-AC 05/29/09 19,015 132 237 Well-AC 06/22/09 19,220 134 240 Well-AC 07/21/09 20.130 142 250 Well-AC 08/27/09 22*826 143 265 Well-AC 09/25/09 21.881 152 266 Well-AC 10/22/09 20.906 139 251 Well-AC 11/18/09 24,489 132 264 Well-AC 12/14/09 27.4'71 146 287 Well-AD 10/27/03 1
244.000l NA NA Well-AD 11/02/03 1
242,000 NA NA Well-AD 11/17/03 1
225,001 NA NA Well-AD 12/04/03 1
492.
NA NA Well-AD 12/04/03 1
,392,001 NA NA Well-AD 12/16/03 1
- 487,000 NA NA Well-AD 12/16/03 1
- 490, NA NA Well-AD 01/14/04 1
220,000 NA NA Well-AD 02/17/04 1
400000 NA NA Well-AD 03/03/04 1
420000A A
Well-AD 04/06/04 1
542,000
(
4,706 10,418 Well-AD 05/04/04 1
624,000 5,589 11,649 5.8 65 Well-AD 05/11/04 1
599600 5,392 11,469 Well-AD 05/19/04 1
610,000, 5,780 11,152
<3.3 109 Notes.
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
[
onstituent was detected above its New Jersey Groundwater Quality Criteria.
N ot Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 45 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium IaIo Major Cations and Anions Identification Date INote kResult (pCi/L) ILLD Deviation IBoron(mg/L) ISodinm(mgfL)
Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD 06/03/04 06/17/04 07/07/04 07/12/04 07/19/04 07/28/04 08/02/04 08/09/04 08/16/04 12/28/04 03/02/05 03/07/05 03/14/05 03/23/05 03/28/05 04/18/05 05/18/05 06/22/05 07/19/05 08/15/05 10/17/05 11/15/05 12/12/05 01/24/06 02/23/06 03/21/06 04/17/06 05/15/06 06/20/06
'44,060 7869.000 7196000 772,000 1l46,000 704.000 6"L7000; 4,563 5,666 3,360 3,620 2,870 4,280 3,030 4,850 3,320 4,060 3,670 3,490 4,320 3,790 6,280 4,420 3,490 3,750 3,750 3,905 3,790 3,430 4,370 3,550 3,920 3,730 5,510 5,000 4,890 12,461 12,887 11,900 12,300 12,100 12,500 12,600 1,230 13,000 1,130 11,700 11,300 12,100 10,700 3,640 10,000 9,320 8,160 7,610 6,575 7,010 6,700 5,860 5,710 5,640 5,330 5,460 5,780 4,870
<3.3 12.00 12.80 71 81 90 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
E 0ioo Constituent was detected above its New Jersey Groundwater Quality Criteria.
11ýNot Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 46 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample tTritium I
Major Cations and Ano Identification Date INote IResult (pCiIL) ILLD IDeviation IBoron(ing/L) ISodium~gL Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD 07/24/06 08/22/06 09/21/06 10/06/06 11/16/06 12/15/06 01/23/07 02/06/07 03/14/07 06/19/07 07/19/07 08/23/07 09/20/07 10O/17/07 11/15/07 12/13/07 01/24/08 03/12/08 04/23/08 05/09/08 06/12/08 07/16/08 09/22/08 02/18/09 04/29/09 05/11/09 06/10/09 80.300) 81.900K 73,600k K76,143/
72,300 ~
71,973 61,324
~71.300 Well-D 07/4/065,470 4,65 Well-D 08/2/062,520 2,10 Well-D 09/1/067,550 4,24 Well-D 10/6/066,270 4,43 Well-D 11/6/06768951 Well-D 12/5/06747747 Well-AD 01/23/08155 48 Well-AD~~
09200 14643 Well-AD 10/17/07167041 Well-AD5)5ý 111/7 2O5 5,470 2,520 7,550 6,270 168 147 155 4,370 4,020 3,430 4,530 4,280 146 167 123 148 140 146 5,060 148 5,210 4,780 134 NA 149 4,610 4,540 4,650 2,100 4,240 4,430 517 471 481 4,130 3,770 4,300 4,200 4,520 431 416 351 376 372 416 4,090 105 3,980 4,060 394 NA 108 4,640 3,950
=
a~a.
a a
S.
Well-AE 10/27/03 I
5,990 145 156 0.23 14 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
Constituent was detected above its New Jersey Groundwater Quality Criteria.
N ot Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 47 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium
-1o Major Cations and Anions Identification Date INote lResult (pCi/L) I LLD IDeviation IBoron(mgfL) ISodium~ng/L)
Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE 11/02/03 11/19/03 12/04/03 12/18/03 12/18/03 01/14/04 02/09/04 02/09/04 03/03/04 03/18/04 04/28/04 05/03/04 06/17/04 07/13/04 08/16/04 09/22/04 10/18/04 11/22/04 12/16/04 01/18/05 02/08/05 03/08/05 04/11/05 05/10/05 06/07/05 07/06/05 08/02/05 09/07/05 10/04/05 5,710 6,910 10,200 15,800 16,100 16,100 16,600 19,200 17,000 19,000 14,900 14,000 7,810 7,820 7,238 5,939 5,375 4,636
-3,230 7,530 10,100 13,026 8,832 9,305 7,741 6,336 4,947 3,384 3,305 NA NA 146 147 NA 144 139 NA 147 145 140 5,589 5,666 149 151 140 150 152 3,230 164 147 142 157 147 147 148 148 150 152 NA NA 190 229 NA 229 232 NA 237 248 220 2,409 2,152 175 173 156 156 149 1,200 185 192 212 192 187 173 162 149 134 135 0.17 0.09
<3.33 0.099 10 8
11 11 Notes:
LLD mg/L pCi/L Lower Limit of Detection Milligrams per liter Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
[i2o Constituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 48 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 well Sample TritiunlI Major Cations and Anions Identification Date INote Rlesult (pCiIL) I'LLD IDeviation IBoron(mg/L) ISodinns(mg/]L)
Well-AE Well-AE Well-AE WelI-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE 11/02/05 12/09/05 01/16/06 02/07/06 03/07/06, 04/04/06 05/02/06 06/19/06 07/17/06 08/21/06 09/18/06 10/05/06 11/02/06 12/07/06 01/13/07 02/24/07 03/07/07 04/20/07 05/16/07 06/18/07 07/19/07 08/15/07 09/19/07 10/04/07 11/19/07 12/12/07 01/16/08 02/07/08 03/12/08 1
I 3,592 5,123 9,966 13,400 9,924 7,075 3,945 4,379 3,822 11,860 4,300 5,226 5,000 4,289 5,721 4,749 5,233 8,428 6,863 5,663 5,174 4,064 4,065
,4,673 4,998 7,322 9,715 10,326 151 153 3,550 149 3,310 161 150 151 160 152 167 161 161 172 156 170 143 156 153
'146 146 147 144 158 151 148 140 151 152 136 154 2,390 193 2,000 200 171 141 150 140 219 151 160 167 150 171 146 159 182 164 153 149 137 149 153 148 165 190 196 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
[jjj~
C onstituent was detected above its New Jersey Groundwater Quality Criteria.
1TA-Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 49 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Identification Date Note lResult (pCi/L) I LLD
]Deviation Boron(mg/L) ]Sodium(mg/L)
WeI1-AE 04/01/08 11,548 160 210 WeII-AE 05/08/08 10,692 140 188 WeI1-AE 06/19/08 7,902 134 163 Well-AE 07/16/08 7,569 143 168 Well-AE 08/18/08 6,349 139 155 Well-AE 09/02/08 6,152 134 149 Well-AE 10/17/08 6,302 134 152 WelI-AE 11/18/08 9,085 133 174 Well-AE 12/16/08 10,576 149 194 Well-AE 01/09/09 11,859 151 204 Well-AE 02/24/09 149 256 WelI-AE 03/16/09 23390 145 267 Well-AE 04/01/09 23 134 254 WelI-AE 05/13/09 12,382 145 202 Well-AE 06/03/09 11,056 132 188 Well-AE 07/21/09 9,805 141 184 WelI-AE 08/18/09 8,054 145 173 WelI-AE 09/23/09 5,939 149 157 WelI-AE 10/22/09 6,216 139 154 Well-AE 11/04/09 6,147 132 149 WelI-AE 12/22/09 5,409 143 148 Well-AF 10/07/03
-142 142 86 0.38 227 Well-AF 10/27/03 242 145 90 Well-AF 10/27/03 1
-2,430 2,430 NA WelI-AF 11/10/03 330 144 91 Well-AF 11/24/03 245 146 91 0.43 545 Well-AF 12/10/03 343 140 89 Well-AF 12/22/03 302 141 89 Notes:
LLD mg/L Lower Limit of Detection Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
F ooi Constituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 50 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium Io Major Cations and Anions Identification Date INote ýResult (pCi/L,) I LLD IDeviation IBoron(mg/L) ISodium(mg/L)
Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF 01/06/04 01/20/04 02/02/04 03/18/04 04/20/04 05/03/04 06/25/04 07/13/04 08/16/04 09/23/04 10/12/04 11/16/04 12/21/04 01/11/05 02/08/05 03/14/05 04/11/05 05/09/05 07/11/05 10/17/05 01/16/06 04/10/06 07/17/06 10/09/06 01/22/07 04/19/07 07/13/07 10/09/07 01/23/08 1
1 366 262 295 150 247 308 301 270 177 241
-151 168
-3,910
-3,910
-154
-4,320 363 245 193 182 264 244 372 249 347 223 210
-173 158 142 143 144 144 141 141 144 145 156 147 151 153 3,910 3,910 154 4,320 148 143 152 157 152 156 154 162 158 165 146 173 139 90 89 91 88 88 89 90 91 96 92 90 94 1,130 1,180 94 1,240 94 89 93 96 95 97 97 100 99 102 90 101 85 4.80E-01 0.523 0.644 654 766 843 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
[
Constituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 51 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample I
Tritium Major Cations and An Identification Date Note Result (pCiIL)I LLD Deviation Boron(mg/L)
Sodium(mg/L)
Well-AF 04/22/08
-154 154
.93 Well-AF 07/16/08 177 143 88 Well-AF 10/20/08 4137 137 81 Well-AF 01/19/09
,141 141 85 WelI-AF 04/08/09 252 146 91 WelI-AF 07/21/09 259 140 88 WelI-AF 10/20/09 143 143 87 WeI1-AG-D 02/23/04 6,100 140 156 0.34 849 WelI-AG-D 03/09/04 3,280 149 132 Well-AG-D 03/29/04 2,540 151 125 Well-AG-D 04/12/04 4,990 141 145 5.10E-01 765 WelI-AG-D 04/19/04 2,920 141 124 0.5 868 Well-AG-D 04/28/04 896 135 95 0.38 866 WelI-AG-D 05/03/04 1
'5,590 5,590 NA WelI-AG-D 05/10/04 1,490 140 106 5.60E-01 885 WelI-AG-D 05/24/04 1,290 152 109 Well-AG-D 05/28/04 1
'4,560 4,560 1,551 Well-AG-D 06/03/04 4,040 145 139 Well-AG-D 06/08/04 13,625 142 214 Well-AG-D 06/16/04 566 154 101 0.18 239 Well-AG-D 06/25/04 1,865 141 111 0.539 862 Well-AG-D 07/07/04 2,698 141 121 Well-AG-D 07/14/04 3,426 142 130 0.506 798 WelI-AG-D 07/19/04 2,718 152 128 Well-AG-D 07/28/04 2,939 145 127 0.518 826 Well-AG-D 08/09/04 4,217 148 143 0.533 883 Well-AG-D 08/23/04 6,538 156 171 WelI-AG-D 09/13/04 7,191 149 172 Notes:
LLD mg/L pCi/L Lower Limit of Detection Milligrams per liter Picocuries per liter 1
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
[2 onstituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 52 of 93 0
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample I
Tritium Io Major Cations and Anions Identification Date INote lResult (pCi/L) ILLD IDeviation IBoron(mg/L) ISodium(mg/L)
WelI-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D WeUI-AG-D Well-AG-D Well-AG-D WeI1-AG-D WeII-AG-D Well-AG-D WeII-AG-D WeII-AG-D WeII-AG-D WelI-AG-D WelI-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D WelI-AG-D WelI-AG-D WelI-AG-D WelI-AG-D WeII-AG-D Well-AG-D 09/29/04 10/05/04 10/18/04 11/04/04 11/09/04 11/15/04 11/22/04 11/29/04 12/07/04 12/14/04 12/21/04 12/28/04 01/07/05 01/11/05 01/18/05 01/26/05 02/02/05 02/09/05 02/14/05 02/22/05 03/03/05 03/07/05 03/14/05 03/23/05 03/28/05 04/05/05 04/18/05 05/03/05 05/16/05 13,241 8,613 12,456 7,424 11,993 3,813 8,860
-4,170 6,910
-3,910 5,710 6,300 8,700 4,880 4,040 6,455 6,310 5,995 958 1,099 937 1,026 1,203 1,217 764 938 1,380 798 148 156 144 139 3,230 150 148 2,650 4,170 3,230 3,910 4,060 150 143 154 141 155 149 146 155 148 155 143 149 141 169 162 149 144 218 190 209 167 2,690 209 138 1,580 1,510 1,500 1,370 1,570 166 180 153 139 168 162 159 107 105 106 101 107 102 113 111 109 98 0.823 0.39 0.344 836 1,060 971 958 876 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
2 onstituent was detected above its New Jersey Groundwater Quality Criteria.
50qot Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 53 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample ITritiums Major Cations and Anions Identification Date Note Result (pCi/L)I LLD Deviation Boron(mg/L)
Sodium(mg/L)
Well-AG-D 06/06/05 883 148 102 929 Well-AG-D 07/11/05 884 149 102 858 Well-AG-D 08/01/05 762 144 97 865 Well-AG-D 09/06/05 1,170 149 106 Well-AG-D 10/11/05 901 147 101 WelI-AG-D 11/01/05 995 150 104 Well-AG-D 12/08/05 712 146 98 WelI-AG-D 01/09/06 525 156 101 Well-AG-D 02/06/06 575 177 114 Well-AG-D 03/06/06 620 159 104 Well-AG-D 04/03/06 270 156 97 WelI-AG-D 05/01/06 486 152 99 Well-AG-D 06/05/06 685 155 102 Well-AG-D 07/11/06 763 162 108 WelI-AG-D 08/07/06 720 153 102 WelI-AG-D 09/18/06 663 158 104 Well-AG-D 10/06/06 413 160 101 Well-AG-D 11/15/06 671 160 106 WelI-AG-D 12/08/06 496 198 126 Well-AG-D 01/14/07 543 159 103 Well-AG-D 02/20/07 204 158 97 Well-AG-D 03/14/07 201 179 110 Well-AG-D 04/19/07 391 175 111 Well-AG-D 05/03/07 633 141 94 WeII-AG-D 06/18/07 716 142 95 WeI1-AG-D 07/12/07 490 151 97 Well-AG-D 08/16/07 702 147 98 Well-AG-D 09/20/07 608 144 95 WelI-AG-D 10/17/07 2,172 149 118 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
Fiio Constituent was detected above its New Jersey Groundwater Quality Criteria.
NXNot Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 54 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 well Sample Tritium Major Cations and Anions Identification I
Date Note [Result (pCi/L) I LLD Deviation Boron(mg/L)
Sodiuns(mg/L)
Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D WeII-AG-D Well-AG-D WeUl-AG-D WelI-AG-D WelI-AG-D Well-AG-D WelI-AG-D Well-AG-D WelI-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D 11/20/07 12/20/07 01/23/08 02/20/08 03/13/08 04/01/08 05/15/08 06/24/08 07/17/08 08/18/08 09/03/08 10/17/08 11/21/08 12/23/08 01/20/09 02/18/09 03/16/09 04/22/09 05/13/09 06/03/09 07/22/09 08/19/09 09/24/09 10/21/09 11/04/09 12/29/09 1,491 905 1,019 1,116 1,141 1,153 1,724 1,974 1,536 1,205 1,120 1,367 882 1,070 1,023 499 2,182 1,094 909 747 462 1,235 1,110 999 1,134 1,084 150 137 154 153 137 149 135 136 138 134 134 132 131 134 133 141 143 146 144 135 141 154 138 139 132 143 113 96 106 107 99 106 105 109 104 98 96 99 91 96 95 92 115 103 99 92 91 110 99 98 95 101 12/29/09 1,084 143 101 Well-AG-S 02/23/04 2,320 138 f
115 1 0.04 348 Well-AG-S 03/09/04 3,000 146 126 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
[
W
ý Constituent was detected above its New Jersey Groundwater Quality Criteria.
0;WNot Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 55 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) I LLD I
Deviation Boron(mg/L) I Sodium(mg/L)
Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S 03/29/04 04/12/04 04/20/04 04/28/04 05/10/04 05/24/04 05/26/04 05/27/04 05/28/04 06/03/04 06/08/04 06/16/04 06/25/04 07/07/04 07/14/04 07/19/04 07/26/04 07/28/04 07/30/04 08/09/04 08/23/04 09/13/04 09/29/04 10/05/04 10/18/04 11/04/04 11/09/04 11/15/04 11/22/04 4,810 6,620 8,060 10,300 9,580 9,390 11,300 18,300 14,400 17,329 13,226 17,244 13,528 17,361 12,601 15,617 i00 10,430 7,074 11,088 16,353 15,313 Lu.i00 LIL20 153 143 142 136 139 147 5,780 4,563 4,563 150 154 145 152 147 149 149 3,230 147 4,850 144 3,025 151 160 154 143 150 3,230 3,910 4,220 150 161 173 188 184 189 2,281 2,383 2,193 242 220 237 263 217 241 210 2,230 232 2,700 263 2,176 200 179 207 233 231 2,320 2,390 2,350 0.26 0.23 0.19 319 338 312 0.247 0.271 0.243 0.231 0.241 286 300 323 341 315 365 321 Notes:
LLD mg/L pCi/L Lower Limit of Detection Milligrams per liter Picocuries per liter 1
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
Fnýi:] Constituent was detected above its New Jersey Groundwater Quality Criteria.
-NKNot Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 56 of 93 0
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium Major Cations and An Identification Date Note Result (pCi/L) I LLD Deviation Boron(mg/L) I Sodium(mg/L)
Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S 11/29/04 12/07/04 12/14/04 12/21/04 12/28/04 01/07/05 01/11/05 01/18/05 01/26/05 02/02/05 02/02/05 02/09/05 02/14/05 02/22/05 03/03/05 03/07/05 03/14/05 03/23/05 03/28/05 04/05/05 04/18/05 05/03/05 05/16/05 06/06/05 07/11/05 08/01/05 09/06/05 10/11/05 11/01/05 21,300 23,300 23,701) 92,2 0 0 28,800 29,400 29,370 31,2007 11,929 6,944 7,239 7,693 9,248 9,399 9,357 3,472 6,858 2,493 1,007 2,022 3,537 4,295 6,309 4,043 2,650 4,170 3,230 4,020 4,060 3,910 3,910 3,950 149 4,660 2,650 4,660 3,910 154 158 136 143 147 141 143 152 151 146 148 150 151 151 146 149 2,220 2,480 2,330 2,700 2,380 2,610 2,770 2,630 267 2,810 2,660 2,710 2,480 211 174 164 171 187 183 187 138 169 121 103 119 136 144 160 139 0.175 0.144 240 426 236 192 567 582 606 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
20,00 Constituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 57 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample I
Tritium I
Major Cations and Anionum Identification IDate INote [Result (pCi/L) ILLD IDeviation IBoron(mg/)
I Sodium(mg/I)
I Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S 12/08/05 01/09/06 02/06/06 03/06/06 04/03/06 05/01/06 06/05/06 07/11/06 08/07/06 09/18/06 10/06/06 11/15/06 12/08/06 01/14/07 01/22/07 02/20/07 03/14/07 04/19/07 05/03/07 06/18/07 07/12/07 08/16/07 09/20/07 11/20/07 12/20/07 01/23/08 02/20/08 03/13/08 04/01/08 349 744 1,551 1,926 1,616 1,150 639 499 453 403 339 602 487 513
-4,610 406 336 363 201 888 645 1,101 671 304 343 291 432 341 320 150 159 165 157 159 149 158 162 158 159 165 158 194 157 4,610 152 190 160 142 141 150" 144 146 142 137 151 151 139 144 95 106 121 120 118 106 103 104 101 101 103 104 123 102 NA 97 118 101 88 97 99 102 97 90 87 94 96 88 91 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
2 Constituent was detected above its New Jersey Groundwater Quality Criteria.
N ot Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 58 of 93 0
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample ITritium Major Cations and Anion Identification Date Note Result (pCi/L)
Sodium(mg/L)
Well-AG-S 05/15/08 383 147 93 Well-AG-S 06/24/08 633 136 91 Well-AG-S 07/17/08 653 138 92 Well-AG-S 07/21/08 1
'4,780 4,780 NA Well-AG-S 08/18/08 590 133 88 Well-AG-S 09/03/08 537 134 88 Well-AG-S 10/17/08 1,074 133 95 Well-AG-S 11/21/08 1,580 131 101 Well-AG-S 12/23/08 2,405 143 119 Well-AG-S 01/20/09 3,107 140 125 Well-AG-S 02/18/09 1,936 133 107 Well-AG-S 03/16/09 1,970 143 112 Well-AG-S 04/22/09 1,236 142 103 Well-AG-S 05/13/09 913 143 99 Well-AG-S 06/03/09 773 134 92 Well-AG-S 07/22/09 620 137 91 Well-AG-S 08/19/09 1,230 150 107 Well-AG-S 09/24/09 1,368 135 100 Well-AG-S 10/21/09 1,240 140 102 Well-AG-S 11/04/09 1,337 132 98 Well-AG-S 12/29/09 1,007 144 100 Well-AH-D 02/23/04 548 142 93 0.21 309 WelI-AH-D 03/08/04 620 142 95 Well-AH-D 03/29/04 522 142 93 0.31 290 Well-AH-D 04/19/04 563 140 93 0.19 241 Well-AH-D 05/03/04 637 142 95 Well-AH-D 06/03/04 619 157 103 Well-AH-D 06/16/04 1
-5,670 5,670 1,571 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
i Constituent was detected above its New Jersey Groundwater Quality Criteria.
N'Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 59 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 well Sample Tritium I
Major Cations and Anions Identification Date INote ýResult (pCi/L)
LLD IDeviation IBoron(nsglL) ISodinns(mg/L)
Well-AH-D Well-AH-D Well-AH-D Well-AH-D Well-AH-D Well-AH-D Well-AH-D Well-AH-D Well-AH-D Well-AH-D Well-AH-D Well-AH-D Well-AH-D Well-AH-D Well-AH-D Well-AH-D Well-AH-D Well-AH-D Well-AH-D WelI-AH--D Well-AH-D Well-AH-D Well-AH-D WeII-AH-D Well-AH-D Well-AH-D Well-AH-D Well-AH-D Well-AH-D 07/19/04 08/23/04 09/13/04 09/29/04 10/18/04 11/15/04 12/20/04 01/11/05 02/15/05 03/08/05 04/18/05 05/16/05 06/07/05 07/11/05 08/02/05 09/07/05 10/17/05 11/02/05 12/09/05 01/10/06 02/06/06 03/06/06 04/10/06 05/01/06 06/05/06 07/17/06 08/08/06 09/06/06 10/06/06 I
I 552 586 557 517 308
'3,910
'3,910 487 493 529 407 492 610 665 599 522 361 403 257 260 264 318 303 439 297 321 330 322 278 147 140 151 155 144 3,910 3,910 154 147 146 150 146 148 143 145 151 156 152 151 151 165 156 155 152 157 160 157 161 162 97 93 99 101 90 1,328 1,130 100 96 96 96 95 98 96 96 98 99 97 94 94 102 98 97 98 98 100 98 101 101 0.191 0.235 0.298 260 250 673 654 1,020 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
[ii Constituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 60 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample I
Tritium Io Major Cations and Anions Identification Date INote lResult (pCi/L) I'LLD IDeviation IBoron(mgfL) ISodium(mgIL)
Well-AH-D Well-AH-D WoIl-AH-D WaIl-AH-D WIl-AH-D WOI-AH-D WcIl-AH-D Wll-AH-D WoIl-AH-D Well-AH-D WelI-AH-D WeIl-AH-D Wcll'AH-D WclI-AH-D WcIl-AH-D WelI-AH-D WclI-AH-D WeIl-AH-D Well-AH-D Wll-AH-D WeII-AH-D W4I-AH-D WelI-AH-D WlI-AH-D W0II-AH-D WlII-AH-D WeI-AH-D WdII-AH-D WelI-AH-D 11/02/06 12/19/06 01/22/07 02/20/07 03/14/07 04/19/07 05/15/07 06/18/07 07/13/07 08/15/07 09/19/07 10/03/07 11/19/07 12/12/07 01/23/08 02/07/08 03/12/08 04/01/08 05/29/08 06/20/08 07/07/08 08/18/08 09/22/08 10/17/08 11/18/08 12/16/08 01/09/09 02/18/09 03/16/09 430 209 333
-177 155 270
-142 343 221 1,089 376 1,311 920 973 1,104 1,209 1,524 1,799 1,675 1,265 1,010 729 751 741 809 489 690 280 1,440 152 159 159 177 155 168 142 141 149 148 145 151 177 138 152 150 146 148 136 136 139 131 141 137 132 133 136 147 143 97 98 100 108 94 104 86 89 92 104 92 109 119 97 106 107 109 113 105 99 98 89 95 93 91 87 92 92 106 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
j Constituent was detected above its New Jersey Groundwater Quality Criteria.
N7 Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 61 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L)
Sodium(mg/L)
Well-AH-D 04/22/09 298 140 88 Well-AH-D 05/11/09 644 137 92 Well-AH-D 06/03/09 415 132 85 Well-AH-D 07/21/09
-141 141 85 Well-AH-D 08/04/09
-145 145 87 Well-AH-D 09/02/09
-136 136 82 Well-AH-D 10/08/09 198 142 87 Well-AH-D 11/04/09 209 133 83 Well-AH-D 12/29/09 293 149 93 Well-AH-S 02/23/04 899 143 99 0.14 135 Well-AH-S 03/08/04 894 142 98 Well-AH-S 03/29/04 878 141 97 0.27 56 Well-AH-S 04/20/04 932 141 98 0.25 67 Well-AH-S 05/03/04 908 141 98 Well-AH-S 06/03/04 759 149 100 Well-AH-S 06/16/04 835 142 97 0.263 48 Well-AH-S 07/19/04 816 151 103 0.204 38 Well-AH-S 08/23/04 752 155 105 Well-AH-S 09/13/04 512 144 94 Well-AH-S 09/29/04 533 149 97 Well-AH-S 10/18/04 420 159 101 Well-AH-S 11/15/04 1
,3,910 3,910 1,235 Well-AH-S 12/20/04 1
'3,910 3,910 1,130 Well-AH-S 01/11/05 658 163 107 0.446 61 Well-AH-S 02/15/05 633 146 97 Well-AH-S 03/08/05 614 147 97 Well-AH-S 04/18/05 319 146 92 0.138 216 Well-AH-S 05/16/05 249 150 93 277 0
s Notes:
LLD mg/L pCi/L Lower Limit of Detection Milligrams per liter Picocuries per liter 1
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
[-2 Constituent was detected above its New Jersey Groundwater Quality Criteria.
Nq Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 62 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 well Sample Tritium Major Cationm a Aons Idniicto at oeResult (pCi/L) ILLD IDeviation Boron(mg/L) ISodium(mg/L)
Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S 06/07/05 07/11/05 08/02/05 09/07/05 10/17/05 11/02/05 12/09/05 01/10/06 02/06/06 03/06/06 04/10/06 05/01/06 06/05/06 07/17/06 08/08/06 09/06/06 10/06/06 11/02/06 12/1 9/06 01/22/07 02/20/07 03/14/07 04/19/07 05/15/07 06/18/07 07/13/07 08/15/07 09/19/07 10/03/07 238 293 241 162
'153 298 218 251 213
-158
-155 163 190 171 178 211 238 366 252 384 242 248
-162 154 236 1,193
-145
'144 195 147 144 147 149 153 151 148 153 170 158 155 151 156 171 160 157 159 154 163 155 151 149 162 137 142 147 145 144 164 91 91 92 91 92 94 91 95 105 94 92 92 96 104 98 97 99 97 101 98 93 93 98 84 88 105 88 88 101 151 Notes_
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
F-2, o6Constituent was detected above its New Jersey Groundwater Quality Criteria.
N ot Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 63 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium Major Cationa and Anions Identification Date Note Result (pCi/L)
Sodium(mg/L)
Well-AH-S 11/19/07 2,790 190 152 WelI-AH-S 12/12/07 5,579 142 150 Well-AH-S 01/23/08 1,322 152 109 Well-AH-S 02/07/08 1,365 139 103 Well-AH-S 03/12/08 1,377 145 107 Well-AH-S 04/01/08 400 142 91 Well-AH-S 05/29/08 274 148 92 Well-AH-S 06/20/08 546 136 89 Well-AH-S 07/07/08 434 138 89 Well-AH-S 08/18/08 488 132 87 Well-AH-S 09/22/08 620 128 86 Well-AH-S 10/17/08 738 133 91 Well-AH-S 11/18/08 1,345 131 98 Well-AH-S 12/16/08 858 139 96 Well-AH-S 01/09/09 749 137 93 Well-AH-S 02/18/09 157 157 96 Well-AH-S 03/16/09 567 144 94 Well-AH-S 04/22/09 421 142 91 Well-AH-S 05/11/09 402 137 88 Well-AH-S 06/03/09
-132 132 77 Well-AH-S 07/21/09
,143 143 86 Well-AH-S 08/04/09
,142 142 85 Well-AH-S 09/02/09
,134 134 79 Well-AH-S 10/08/09
,135 135 80 Well-AH-S 11/04/09
-132 132 77 Well-AH-S 12/29/09 153 153 90 Well-Al 02/02/04 1
5,780 15,780 NA
-0 Well-Al 02/26/04 4,360 1
140 1
138 0.058 0
Notes:
LLD mg/L pCi/L Lower Limit of Detection Milligrams per liter Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
[i2000o Constituent was detected above its New Jersey Groundwater Quality Criteria.
Ný Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 64of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Date I
Matoronsmg nd ions Identification IDate I Note R--tET
-FB IDvainIornm/)ISdumgL Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al 03/11/04 03/30/04 05/04/04 05/11/04 05/19/04 06/03/04 07/19/04 07/28/04 08/02/04 08/09/04 08/16/04 08/25/04 12/27/04 04/19/05 05/10/05 06/21/05 07/12/05 08/15/05 09/06/05 10/10/05 11/14/05 12/20/05 01/17/06 02/21/06 03/20/06 04/10/06 04/11/06 05/16/06 06/19/06 4,370 3,550 11,800 45,900L 13,120 13,120 14,060 7,683 6,669 5,081 4,535 3,602 2,755 2,730 4,200
-4,720 5,194 2,354 2,082 145 143 140 5,392 5,780 4,563 2,870 3,790 3,320 4,850 3,320 3,030 153 153 3,620 3,750 155 147 150 148 152 156 150 149 3,730 4,720 157 149 162 141 131 200 3,466 3,439 3,360 2,550 2,650 2,670 3,030 3,000 3,050 222 222 2,640 2,820 226 172 166 151 148 139 127 126 1,530 NA 156 122 126 0.17
<3.3 16 47 28 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
_[ýConstituent was detected above its New Jersey Groundwater Quality Criteria.
N ot Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 65 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L)
Sodium(mglL)
Well-Al 07/18/06 1,572 150 112 Well-AI 07/19/06 1
,4,890 4,890 NA Well-A]
08/08/06 1,621 160 118 Well-Al 09/18/06 1,782 157 119 Well-Al 10/10/06 2,110 159 124 Well-Al 11/01/06 1,543 157 116 Well-Al 12/18/06 2,495 178 142 Well-Al 12/19/06 1
-4,840 4,840 NA Well-Al 01/13/07 2,784 149 127 Well-Al 02/06/07 2,393 157 127 Well-Al 03/08/07 2,100 149 119 Well-Al 04/20/07 2,677 161 134 Well-Al 05/15/07 2,556 140 119 Well-Al 06/18/07 2,867 142 123 Well-Al 07/18/07 2,784 145 123 Well-Al 08/15/07 3,204 143 128 Well-Al 09/20/07 3,137 150 131 Well-Al 10/03/07 3,360 149 132 Well-Al 11/14/07 3,173 154 138 Well-Al 12/12/07 2,902 138 121 Well-Al 01/17/08 2,933 151 128 Well-Al 02/06/08 2,920 138 122 Well-Al 03/18/08 3,035 149 129 Well-Al 04/02/08 3,255 151 132 Well-Al 05/08/08 3,339 146 129 Well-Al 06/19/08 2,708 136 117 Well-Al 07/07/08 2,934 128
.116 Well-Al 08/06/08 2,005 140 111 Well-Al 09/02/08 2,478 136 114 Notes:
LLD mg/L Lower Limit of Detection Milligrams per liter pCi/L Picocuries per liter 1
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
F2 -o7 Constituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 66 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Wenl Sample I
Tritium j
Major Cations and Anis Identification Date Note IResult (pCiL)I LLD I
Deviation Boron(mg/L) I Sodium(mg/L)
Well-Al 11/19/08 3,732 133 127 Well-AT 12/15/08 5,220 151 152 Well-Al 01/08/09 4,312 139 136 Well-Al 02/11/09 4,747 155 149 Well-Al 03/10/09 3,957 134 129 Well-Al 04/08/09 25,971 142 282 Well-Al 05/11/09 7,007 146 163 Well-Al 06/08/09 10,938 136 190 Well-Al 07/21/09 9,743 134 179 Well-Al 08/18/09 8,722 143 177 Well-Al 09/02/09 4,720 147 144 Well-Al 10/08/09 6,468 139 156 Well-Al 11/17/09 6,988 132 156 Well-AI 12/16/09 3,292 152 132 Well-AJ 02/25/04 1,150 142 102 0.62 616 Well-AJ 03/09/04 1,040 140 99 0.68 650 Well-AJ 03/30/04 1,080 146 103 0.62 642 Well-AJ 04/19/04 1,190 139 101 0.67 621 Well-AJ 05/10/04 1,240 142 103 Well-AJ 05/24/04 1,270 158 113 Well-AJ 06/16/04 1,495 148 111 Well-AJ 07/13/04 2,193 142 116 Well-AJ 07/20/04 1,525 152 113 Well-AJ 08/16/04 1,677 141 110 Well-AJ 09/08/04 4,254 152 146 Well-Al 10/18/04 1
54.80 3,230 3,560 Well-AJ 11/16/04 1
193,.001 3,910 6,440 Well-AJ 12/28/04 1
144,00 2,820 5,450 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
F2iooConstituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 67 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample I
Tritium Major Cations and Anions Identification Date Note IResult (pCi/L) I LLD I
Deviation Boron(mg/L) I Sodium(mg(L)
Well-AJ 01/12/05 1 [
,366.01 3,910 8,540 Well-AJ 02/14/05 1
331.000 3,910 8,260 Well-AJ 03/02/05 1
218000 3,670 6,710 Well-Al 03/07/05 1
155.000 3,490 5,670 WeI-AJ 03/14/05 1
1 4,320 6,120 Well-Al 03/23/05 1
70,400 3,790 3,720 Well-Al 03/28/05 1
152,000 6,280 5,880 Well-Al 04/18/05 1
139.001) 4,420 5,490 Well-Al 05/18/05 1
12LOOO 3,490 4,900 Well-AJ 08/15/05 1
3,905 3,877 Well-Al 10/17/05 1
182,000 3,790 6,330 Well-AJ 11/15/05 1
62,300 3,430 3,770 Well-Al 12/12/05 14,370 5,750
-4 Well-Ad 01/24/06 1
51400 3,550 3,520 Well-AJ 02/23/06 1
42.201) 3,920 3,280 Well-Al 03/21/06 1
66.200 3,730 4,120 Well-Al 04/17/06 1
53.200 5,510 4,030 Well-Al 05/15/06 1
44.441 5,000 3,780 Well-AJ 07/24/06 1
41.100 5,470 3,500 Well-Al 08/22/06 1
2 2,520 1,340 Well-Al 06/19/07 p34W 150 329 Well-Al 08/28/08 4,641 140 139 Well-Al 04/29/09 5,067 148 148 Well-Al 05/11/09 22,215 144 259 Well-Al 06/10/09 L4_5.3 1
135 316 S
Well-AL 02/25/04 11 141 1411 83 0.21 60 Well-AL 03/09/04 11 147 147 86 0.20 55 Well-AL 03/30/04 146 146 86 0.22 63 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
f Constituent was detected above its New Jersey Groundwater Quality Criteria.
w tot Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 68 of 93 0
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Date I
MajoroCations andions Identification Date Note IReault pi)I DIBrnm/
ISdumgL Well-AL Well-AL Well-AL Well-AL Well-AL Well-AL Well-AL Well-AL Well-AL Well-AL Well-AL Well-AL Well-AL Well-AL Well-AL Well-AL Well-AL Well-AL Well-AL Well-AL Well-AL Well-AL Well-AL Well-AL Well-AL Well-AL Well-AL Well-AL Well-AL 04/19/04 05/19/04 06/16/04 07/13/04 07/28/04 08/16/04 09/08/04 10/12/04 11/16/04 12/21/04 01/11/05 02/08/05 03/14/05 04/11/05
.05/09/05 07/11/05 10/10/05 01/23/06 04/10/06 07/17/06 10/09/06 01/13/07 04/19/07 07/19/07 10/09/07 01/23/08 04/22/08 07/16/08 10/20/08 1
1
-141
-151
-141
-141
-147
-150
-153
-146
-3,910
-3,910
,157
'157
'146
-158
<150
-154
'148
-153
-165
'154
-162
'153 243 203
-175 366 375 426 396 141 151 141 141 147 150 153 146 3,910 3,910 157 157 146 158 150 154 148 153 165 154 162 153 158 146 175 151 154 142 139 85 89 85 85 88 91 91 85 1,126 1,130 92 92 87 93 88 90 89 91 99 92 97 91 98 90 103 96 98 91 89 0.3 62 0.23 74 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
F-oo Constituent was detected above its New Jersey Groundwater Quality Criteria.
Nq Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 69 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L)
Sodium(mg/L)
Well-AL 01/19/09 568 146 96 Well-AL 04/08/09 441 141 91 Well-AL 06/10/09 452 132 86 Well-AL 07/21/09 598 151 99 Well-AL 10/20/09 686 136 92 Well-AM 02/02/04 1
4, NA NA Well-AM 02/26/04 1
273,000 NA NA Well-AM 02/26/04 1
27,0 NA NA Well-AM 03/11/04 1
- 234,000 NA NA Well-AM 03/11/04 1
23
.000 NA NA Well-AM 04/08/04 1
196,000 5,822 6,425 Well-AM 04/08/04 1
196,000 5,822 6,425 Well-AM 05/06/04 1
[150,001) 5,589 5,807 Well-AM 05/06/04 1
5,589 5,807 Well-AM 05/20/04 1
149,000 4,563 5,651
<3.3 6
Well-AM 06/10/04 1
156,0011 4,974 5,832
<3.33 5
Well-AM 07/20/04 1
128,000 2,870 5,020 Well-AM 08/17/04 1
137,000 3,320 5,270 Well-AM 09/14/04 1
139,000 4,560 5,380 6
Well-AM 10/25/04 1
124,001 3,030 5,080 Well-AM 11/23/04 1
116.000 4,220 4,940 Well-AM 12/27/04 1
103,000 4,060 4,590 Well-AM 01/12/05 1
108'...
3,910 4,660 Well-AM 02/22/05 1
89301) 3,550 "4,340 Well-AM 03/15/05 1
4,320 4,100 Well-AM 04/19/05 1
54,200 4,420 3,570 Well-AM 05/17/05 1
58,400 3,490 3,480 Well-AM 06/21/05 1
a 3,750 3,420 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
20;O00 Constituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
'02/24/2010 11:26 AM Page 70 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Identification Date Note lResult (pCi/) I 'LLD I
Deviation IBoron(mg/L) I SodiummgL Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM 07/11/05 08/15/05 09/20/05 10/10/05 11/14/05 12/20/05 01/23/06 02/23/06 03/21/06 04/11/06 05/16/06 06/20/06 07/17/06 07/21/06 08/08/06 08/21/06 09/07/06 09/13/06 09/19/06 10/09/06 11/01/06 11/15/06 12/07/06 12/18/06 01/13/07 01/22/07 02/06/07 02/23/07 03/08/07 3;87.500 43,101)/
~25,401)>
72.0 429,0002~
866,()()
2554000 17,5003 Ijooi>
18,191 19,530 22037>
20i.493 3,750 3,905 4,563 3,790 3,430 3,430 3,550 3,920 3,730 4,720 5,000 4,890 4,670 NA NA 2,520 151 NA 161 156 162 162 153 148 148 155 162 157 149 3,110 2,979 4,478 2,930 3,210 2,580 2,750 4,200 10,100 13,700 15,100 12,100 5,130 NA NA 3,590 241 NA 257 261 275 290 330 352 266 294 311 407 266 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
F o
Constituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 71 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Identification Date Note lResult (pCi/L) I LLD Deviation Boron(mg/L)
Sodium(mg/L)
Well-AM 04/20/07 160 275 Well-AM 05/15/07 36.032 174 363 Well-AM 06/19/07 1
50.300 3,430 3,730 Well-AM 07/18/07 37.401l 146 335 Well-AM 07/30/07 36,6 139 321 Well-AM 08/15/07
,38.711 148 342 Well-AM 09/21/07 1
209,000 3,830 7,330 Well-AM 09/25/07 1
249,000 3,730 7,950 Well-AM 10/03/07 1
.223,000 3,830 7,550 Well-AM 10/17/07 1
118000 4,370 5,690 Well-AM 11/14/07 1
f101000 4,110 5,210 Well-AM 11/28/07 1
105,000 3,630 5,330 Well-AM 12/12/07 2=2.
150 272 Well-AM 12/27/07 19,329 149 250 Well-AM 01/17/08 18,293 140 239 Well-AM 01/28/08 19,454 140 246 Well-AM 02/06/08 19,910 140 250 Well-AM 02/20/08 19,927 149 255 Well-AM 03/13/08 17,686 146 241 Well-AM 03/18/08 21,764 146 265 Well-AM 04/02/08 25,177 155 287 Well-AM 04/23/08 2S5398 146 282 Well-AM 05/08/08 147 270 Well-AM 06/24/08 22,981 135 256 Well-AM 06/30/08 23,57 136 262 Well-AM 07/07/08 26,203 141 281 Well-AM 07/24/08 21,019 140 253 Well-AM 08/07/08 21,348 140 254 Well-AM 08/21/08 30 128 290 Notes:
LLD mg/L pCi/L Lower Limit of Detection Milligrams per liter Picocuries per liter 1
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
F-2-iij Constituent was detected above its New Jersey Groundwater Quality Criteria.
S NA Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 72 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCiIL)
Sodium(mg/L)
Well-AM 09/02/08 34,763 132 316 Well-AM 09/22/08 3
1 135 312 Well-AM 11/14/08 301046 147 304 Well-AM 11/25/08 2
0 133 278 Well-AM 12/08/08 30,751 134 297 Well-AM 12/23/08 30935 143 303 Well-AM 01/08/09 36,093 139 324 Well-AM 02/25/09 4,1 145 352 Well-AM 03/26/09 3,780 144
- 306, Well-AM 04/16/09 21 146 259 Well-AM 05/20/09 148 340 Well-AM 06/10/09 9,078 134 175 Well-AM 07/21/09 4,0.71 134 351 Well-AM 08/18/09 2 5,61 138 273 Well-AM 09/23/09 3,2 149 305 Well-AM 10/20/09 32,439 139 307 Well-AM
.11/17/09 29.335 132 287 Well-AM 12/16/09
- 35.292 145 322 Well-AN 08/10/04 21.57) 143 263 0.685 32 Well-AN 08/24/04 19,632 155 263 Well-AN 09/14/04 9,150 141 182 0.567 23 Well-AN 10/25/04 8,950 147 185 Well-AN 11/23/04 6,245 144 158 Well-AN 12/29/04 1
-4,020 4,020 1,210 Well-AN 01/12/05 6,180 159 169 Well-AN 03/02/05 1
192,0011 3,670 6,300 Well-AN 03/07/05 1
A171,0(()
3,490 5,940 Well-AN 03/14/05 1
154000 4,320 5,700 Notes:
LLD Lower Limit of Detection mg/L, Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
,ooo]Constituent was detected above its New Jersey Groundwater Quality Criteria.
N ot Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 73 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L)I LLD I
Deviation Boron(mg/L) I Sodium(mg/L)
Well-AN Well-AN Well-AN Well-AN Well-AN Well-AN Well-AN Well-AN Well-AN Well-AN Well-AN Well-AN Well-AN Well-AN Well-AN Well-AN Well-AN Well-AN Well-AN Well-AN Well-AN Well-AN Well-AN Well-AN Well-AN Well-AN Well-AN Well-AN Well-AN 03/23/05 03/28/05 04/18/05 05/18/05 06/22/05 07/19/05 08/15/05 10/17/05 11/1 5/05 12/12/05 01/24/06 02/22/06 02/23/06 03/21/06 04/17/06 05/15/06 06/20/06 07/24/06 08/22/06 09/21/06 10/06/06 11/16/06 12/15/06 01/23/07 02/06/07 08/23/07 09/20/07 10/17/07 11/15/07 1721000" 149,600) 1621001) 3,1690 75,973 111~6,000 76,400~
3,790 6,280 4,420 3,490 3,750 148 3,905 3,790 3,430 4,370 3,550 149 3,920 3,730 5,510 5,000 4,890 5,470 2,520 7,550 161 3,630 158 154 181 143 151 158 4,110 6,030 4,900 5,650 4,920 4,470 479 3,879 4,150 4,860 4,260 4,800 485 4,030 4,630 4,070 4,870 4,730 3,930 2,320 4,720 138 4,680 286 164 404 289 492 381 3,930 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
EIf.ii o Constituent was detected above its New Jersey Groundwater Quality Criteria.
Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 74 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L)
Sodium(mg/L)
Well-AN 12/13/07 1
67 4,030 4,300 Well-AN 03/12/08 1
60<,500o
°:
3,980 3,950 Well-AN 04/23/08 1
7 0
5,060 4,590 Well-AN 05/09/08 4,827 140 141 Well-AN 06/12/08
+/-!J1i -
136 338 Well-AN 07/16/08 458::: :
144 400 Well-AN 08/21/08 1
51A00 4,530' 3,600 Well-AN 09/22/08 25,168 148 278 Well-AN 03/16/09 5,596 145 151 Well-AN 04/29/09 1,161 147 105 Well-AN 05/11/09 1
4,610 4,470 Well-AN 06/10/09
'3_5 95; 149 326 Well-AO 07/29/04 6,739 146 163 Well-AO 08/10/04 2,399 153 125 0.24 27 Well-AO 08/16/04 5,420 146 155 Well-AO 08/24/04 2,225 155 125 Well-AO 09/14/04 2,417 149 123 Well-AO 09/29/04 2,794 152 130 Well-AO 10/25/04 2,706 158 132 Well-AO 11/23/04 2,570 147 123 Well-AO 12/27/04 1
-4,060 4,060 1,370 Well-AO 01/12/05 1,780 166 125 Well-AO 03/02/05 1
15,900 3,670 2,100 Well-AO 03/07/05 1
158.000 3,490 5,710 Well-AO 03/14/05 1
138,00 4,320 5,430 Well-AO 03/23/05 1
120 3,790 6,570 Well-AO 03/28/05 6,395 147 162 Well-AO 11/15/05 1
341700 3,430 2,900 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
[0060Constituent was detected above its New Jersey Groundwater Quality Criteria.
Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 75 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample ITritium T
Ma.jor Cations and Anions Identification Date Note Result (pCi/L) I LLD Deviation Boron(mg/L)
Sodium(mg/L)
Well-AO 12/12/05 1
4,370 3,750 Well-AO 07/24/06 1
- 38,401 5,470 3,410 WelI-AO 08/22/06 1
986001 2,520 2,290 Well-AO 10/06/06 4,190 160 148 Well-AO 11/16/06 24 164 301 WelI-AO 12/15/06 7,629 168 190 Well-AO 01/23/07 5,136 154 154 WelI-AO 04/29/09 3,045 141 124 Well-AP 07/19/04 2,078 148 118 0.06 59 Well-AP 08/09/04 1,455 150 112 0.126 105 Well-AP 08/23/04 1,006 151 106 Well-AP 09/08/04 1,039 148 105 Well-AP 09/22/04 1,679 156 119 Well-AP 10/11/04 777 151 102 WelI-AP 11/22/04 1,531 150 112 0.204 65 WelI-AP 12/14/04 1
-3,230 3,230 984 WelI-AP 01/27/05 1,200 138 102 0.16 134 WelI-AP 02/01/05 2,680 153 128 WelI-AP 03/07/05 1
70,300 3,490 3,970 Well-AP 04/05/05 1
1()0,()(1(/
4,220 4,730 Well-AP 05/02/05 1
94,400 3,320 1,690 Well-AP 06/06/05 1
>16'000 3,460 4,630 Well-AP 06/21/05 1
3,750 3,220 Well-AP 07/06/05 1,968 144 114 WelI-AP 07/19/05 4,563 148 145 Well-AP 08/01/05 1
6,190 3,320 3,640 Well-AP 08/16/05 1
25,500 3,905 2,564 Well-AP 08/29/05 961 151 105 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
2 l6oConstituent was detected above its New Jersey Groundwater Quality Criteria.
N ot Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 76 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample I
Tritium Ia Major Cations and Aniond Identifica tion IDate INote lResult (pCi/L) I'LLD IDeviation IBoron(mg/L) ISodiuminaglL Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP 09/06/05 09/19/05 10/03/05 10/18/05 11/01/05 12/08/05 01/10/06 02/07/06 02/21/06 03/06/06 03/20/06 04/03/06 04/17/06 05/01/06 05/15/06 06/05/06 06/20/06 07/10/06 07/24/06 08/07/06 08/21/06 09/06/06 10/10/06 11/01/06 12/08/06 01/13/07 02/05/07 03/07/07 04/19/07 I
1,196 10,097 12,250 798 14,354 9,723 14,580 9,829 8,860 9,490 8,284 8,316 7,686 5,639 5,681 757 465 2,006 4,405 2,560 5,939 779 5,412 1,086 4,348 1,169 1,059 150 152 4,220 156 149 3,730 152 152 152 161 3,730 155 158 154 158 167 150 157 152 159 153 157 161 153 186 156 151 151 158 107 195 3,530 212 101 2,750 225 191 226 199 1,850 192 184 184 180 167 158 105 98 123 147 128 166 103 179 109 145 109 111 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
[i2uiooiConstituent was detected above its New Jersey Groundwater Quality Criteria.
RA Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 77 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample ItTritium I
Major Cations and Anions Identification IDate INote lResult (pCi/L) ILLD IDeviation IBoron(mg/L) ISodium(mgAIL Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP 05/15/07 06/18/07 07/18/07 08/15/07 09/19/07 10/03/07 11/14/07 12/12/07 01/17/08 02/21/08 03/12/08 04/01/08 05/08/08 06/19/08 07/07/08 08/07/08 09/02/08 10/17/08 11/18/08 12/15/08 01/27/09 02/25/09 03/16/09 04/08/09 05/11/09 06/03/09 07/22/09 08/04/09 09/23/09 781 1,093 1,049 2,730 3,830 3,442 4,025 3,806 1,282 1,225 1,123 1,224 1,130 1,143 831 1,070 936 947 922 1,113 1,125 1,234 1,510 1,141 1,216 1,250 1,371 1,155 1,257 186 145 144 144 161 150 124 137 154 149 138 147 136 143 128 133 133 146 131 144 145 136 145 144 144 139 141 141 136 123 102 101 122 144 133 128 130 110 106 99 105 98 102 89 95 93 101 92 102 102 100 107 102 103 101 104 101 100 S
Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
FiioW' Constituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26AM Page 78 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium i
Major Cations and Anions Identification Date Note IResult (pCi/L)
LLD Deviation Boron(mg/L) I Sodium(mg/L)
Well-AP 10/08/09 1,196 136 98 Well-AP 11/04/09 1,106 132 95I-Well-AP 12/16/09 1,114 149 105 Well-AQ 07/08/04 1
-3,260 3,260 1,094 Well-AQ 07/19/04 217 142 88 0.436 308 Well-AQ 08/09/04 309 152 95 0.57 1,090 Well-AQ 08/23/04 243 147 92 Well-AQ 09/08/04 273 150 94 Well-AQ 09/22/04 213 138 86 Well-AQ 10/26/04 201 144 89 Well-AQ 11/16/04 218 147 91 Well-AQ 12/21/04 1
,4,280 4,280 1,300 Well-AQ 01/27/05 225 135 84 Well-AQ 02/02/05
'148 148 90 0.448 1,100 WelI-AQ 03/14/05 367 145 92 Well-AQ 04/12/05 247 143 89 Well-AQ 05/09/05 248 151 94 Well-AR 07/14/04 1
324.000 3,620 7,980 Well-AR 07/19/04 1
390,000 2,870 8,700 Well-AR 08/09/04 1
464,000 4,850 9,620 6.00 75 Well-AR 08/23/04 1
496,000 3,670 10,000 Well-AR 09/13/04 1
551,000 4,560 10,500 7.10 65 Well-AR 09/30/04 1
582,000 5,780 10,800 Well-AR 10/26/04 1
589.000 3,030 11,000 Well-AR 12/28/04 1
423,00 4,060 9,050 Well-AR 01/27/05 1
2,470 8,140 Well-AR 02/22/05 1
334000 3,550 8,220 Well-AR 03/14/05 1
204,000 4,320 6,510 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
20.Ol, Constituent was detected above its New Jersey Groundwater Quality Criteria.
N ot Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 79 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Identification Date Note IResult (pCi/L) I LLD I
Deviation Boron(mg/L) I Sodium(mg/L)A Well-AR 04/12/05 1
4,220 7,010 Well-AR 05/10/05 1
215,000 3,620 6,420 Well-AR 06/21/05 1
227.000) 3,750 6,670 Well-AR
.;07/19/05 1 1 201,000 2,820 6,310 Well-AR 08/16/05 1
214000 3,905 6,592 Well-AR 09/19/05 1
180.o000o 4,563 6,272 Well-AR 10/10/05 1
140,000 3,790 5,540 Well-AR 11/02/05 1
7199001) 3,030 6,560 Well-AR 12/08/05 1
1.0 3,730 6,090 Well-AR 01/10/06 1
169,000 4,370 6,250 Well-AR 02/06/06 1
F
))
1)0(0 3,090 4,810 Well-AR 03/20/06 1
3,730 3,510 Well-AR 04/10/06 16,572 155 240 Well-AR 05/15/06 12,555 156 215 Well-AR 06/06/06 12,751 162 221 Well-AR 07/17/06 1
S5.700 4,670 5,000 Well-AR 08/08/06 1
72:100 4,440 4,330 Well-AR 09/06/06
[1.554 157 273 Well-AR 10/10/06 12,619 158 216 Well-AR 11/02/06 74.038 169 506 Well-AR 12/18/06
[6.149 155 447 Well-AR 12/19/06 1
59i900 4,840 4,060 Well-AR 01/13/07 1
85.400 3,730 4,700 Well-AR 02/05/07 1
62ý000 4,370 4,350 Well-AR 03/07/07 1
62.300 3,630 4,110 Well-AR 06/18/07 1
8060 3,430 4,620 Well-AR 07/19/07 1
8 4,44).,,1 4,370 4,780 Well-AR 07/23/07 1
82,300 1,840 2,180 Well-AR 08/08/07 1
0' 4,110 4,390 0
S Notes:
LLD mg/L pCi/L Lower Limit of Detection Milligrams per liter Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
[
onstituent was detected above its New Jersey Groundwater Quality Criteria.
Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 80 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample I
Tritium IMajor Cationi Identification Date INote lResult (pCi/L)I LLD IDeviation Boron(mg/L)
Sodium(mgfL)
Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR 08/15/07 09/19/07 09/25/07 10/03/07 10/17/07 11/14/07 11/28/07 12/12/07 12/27/07 01/23/08 02/21/08 03/12/08 04/01/08 05/08/08 06/19/08 07/07/08 08/18/08 09/04/08 09/22/08 10/13/08 10/27/08 11/18/08 11/25/08 12/15/08 12/23/08 01/08/09 02/24/09 03/16/09 04/08/09 1
1 1
12,266 f2900 16,288 15,470 11,194 11,555 12,787 10,362 8,539 8,935 8,735 15,955 2,2......
3579" 24.809 1114259 3,830 3,830 3,730 157 137 4,110 123 146 149 140 139 147 152 146 135 139 129 134 147 135 135 137 132 148 145 152 154 144 134 4,760 3,760 4,170 267 200 3,940 374 373 360 334 313 323 297 272 220 220 256 266 196 194 202 186 168 181 178 231 327 313 343 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
Constituent was detected above its New Jersey Groundwater Quality Criteria.
Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 81 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample I.Tritium Major Cations and Anions Identification Date Note Result (pCi/L)
LLD I
Deviation Boron(mg/L)
Sodium(mg/L)
Well-AR 05/11/09 1
6.5Oi 4,610 4,240 Well-AR 06/03/09 41,099 131 336 Well-AR 07/21/09 34,407 138 318 Well-AR 08/20/09 I'>!
140 296 Well-AR 09/02/09 150 306 Well-AR 10/21/09 40,987 139 343 Well-AR 11/06/09 3118 132 295 Well-AR 12/22/09 23,314 145 267 Well-AS 07/08/04 1
37,700 3,620 2,920 Well-AS 07/19/04 1
2,870 2,460 Well-AS 08/09/04 1
7,510 4,850 1,920 Well-AS 08/23/04 1
4 3,030 2,990 Well-AS 09/13/04 20,456 145 259 0.727 199 Well-AS 09/29/04 18,171 146 248 Well-AS 10/11/04 9,899 156 200 Well-AS 11/16/04 1
14,400 3,910 2,090 Well-AS 12/21/04 1
15,200 3,910 2,070 Well-AS 01/27/05 14,000 143 224 0.459 186 Well-AS 03/02/05 1
23* 4*0O 3,670 2,430 Well-AS 03/07/05 1
4
,10 3,490 3,020 Well-AS 03/14/05 1
12,600 4,320 2,080 Well-AS 03/23/05 1
72,400 3,790 4,050 Well-AS 03/28/05 1
67.600 6,280 4,180 Well-AS 04/18/05 1
75,700 4,420 4,140 Well-AS 05/18/05 1
59,200 3,490 3,520 Well-AS 06/22/05 1
64,900 3,750 3,730 Well-AS 07/19/05 1
2,820 3,530 Well-AS 08/15/05 1
49jw)*
3,905 3,334 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
Constituent was detected above its New Jersey Groundwater Quality Criteria.
N ot Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
S 02/24/2010 11:26 AM Page 82 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium major Cations and Anions Identification Date Note Result (pCi/L) I LLD I
Deviation Boron(mg/L) I Sodium(mgiL)
Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS 10/17/05 11/15/05 12/12/05 01/24/06 02/23/06 03/21/06 04/17/06 05/15/06 06/20/06 07/24/06 08/22/06 09/21/06 10/06/06 11/16/06 12/15/06 01/23/07 02/06/07 03/14/07 06/19/07 07/19/07 08/23/07 09/20/07 10/17/07 11/15/07 12/13/07 01/24/08 02/25/08 03/12/08 04/23/08
~66,50 61,4O01)
~501900V~
<46,200 iLýL 61,300' 48,104 48,552 32,517*
41,901~"
aml 4,925 14,497 13,072 8,922 15,870 27,876 27,445 ~
25,791 15,043 3,790 3,430 4,370 3,550 3,920 3,730 5,510 5,000 4,890 5,470 2,520 7,550 6,270 163 151 158 162 165 147 146 141 149 168 124 150 141 149 148 160 3,010 3,910 3,870 4,150 4,190 3,640 3,820 3,850 3,970 3,640 1,850 4,350 4,260 584 394 403 334 383 298 146 218 214 204 220 296 326 294 286 233 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
[
C onstituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 83 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L)
Sodium(mg/L)
Well-AS 05/09/08 2,435 137 115 Well-AS 07/16/08 1
5)3 4,780 3,800 Well-AS 08/28/08 6,876 128 154 Well-AS 09/22/08 27_9 145
.288 Well-AS 04/29/09 20 148 259 Well-AT 07/02/04 1
30,60 3,490 2,650 7
Well-AT 07/08/04 4,288 142 139 0.275 309 Well-AT ->
07/12/04 1
32,700 3,620 2,750 Well-AT 07/22/04 1
21 2,870 2,200 Well-AT 08/03/04 1
28,700 3,320 2,580 Well-AT 08/11/04 1
23,00 3,030 2,320 Well-AT 08/12/04 1
3 3,030 2,620 Well-AT 08/13/04 1
@. 20,700 >4:
3,030 2,220 Well-AT 08/21/04 1
w2i70 3,030 2,460 Well-AT 08/31/04 17,124 157 250 Well-AT 12/28/04 1
-4,060 4,060 1,260 Well-AT 01/19/05 1,991 159 124 0.286 163 Well-AT 03/02/05 1
3,670 3,030 Well-AT 03/07/05 1
21200 3,490 2,330 Well-AT 03/14/05 1
40 4,320 3,660 Well-AT 03/23/05 10,039, 150 195 Well-AT 03/28/05 7,973 148 176 Well-AT 04/18/05 4,974 151 153 0.267 396 Well-AT 05/18/05 3,451 151 136 Well-AT 06/22/05 1,777 145 112 Well-AT 07/19/05 1,687 146 112 Well-AT 08/15/05 1,578 150 112 Well-AT 10/17/05 2,224 157 124 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
,Io7 Constituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 84 of 93 S
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium Ia Major Cations and Anions Identification IDate INote ýResult (pCi/L) ILLD IDeviation IBoron(ing/L) ISodium(mgfL)
Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT 11/15/05 12/12/05 01/24/06 02/22/06 02/23/06 03/21/06 04/17/06 05/15/06 06/20/06 07/24/06 08/22/06 09/21/06 10/06/06 11/16/06 12/15/06 01/23/07 02/06/07 03/14/07 04/24/07 05/22/07 06/19/07 07/19/07 08/22/07 08/23/07 09/20/07 10/17/07 11/15/07 12/13/07 03/12/08 1,451 1,722 2,139 2,375
-3,920
-3,730 1,396
.1,517 1,911 2,110 3,715 4,002 4,785 6,235 2,458 2,103 1,401 2,359 4,046 3,482 1,892 2,158
<4,280 2,182 2,114 1,705 2,221 4,326 151 153 153 152 3,920 3,730 159 156 151 151 152 158 159 170 166 146 149 197 160 151 143 145 4,280 148 148 149 176 140 4,890 112 116 121 123 NA NA 115 115 117 120 139 145 154 178 134 118 110 152 149 135 112 116 NA 118 118 112 136 137 3,700 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemislry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
[
Constituent was detected above its New Jersey Groundwater Quality Criteria.
N ot Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 85 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample I
Tritium Major Cations and An Identification Date Note Result (pCi/L)I LLD I
Deviation Boron(mg/L)
Sodium(mg/L)
Well-AT 04/23/08 1
7000 5,060 4,490 Well-AT 05/09/08 14,174 136 210 Well-AT 08/28/08 707 139 94 Well-AT 12/18/08 3,250 132 121 Well-AT 01/19/09 3,158 135 122 Well-AT 03/16/09 3,367 129 120 Well-AT 04/22/09 4,429 135 135 Well-AT 05/11/09 3,891 147 136 Well-AT 06/10/09 2,912 133 118 Well-AV 07/20/05 3,060 NA NA Well-AY 07/20/05 3,000 NA NA Well-AZ 07/20/05 8,710 NA NA Well-BA 10/16/06
'157 157 94 Well-BA 04/10/07 126 126 75 Well-BA 05/07/07 172 172 105 Well-BA 10/17/07
-150 150 89 Well-BA 04/17/08
'147 147 88 Well-BA 10/20/08
'133 133 78 Well-BA 04/13/09
'138 138 83 Well-BA 10/21/09
-138 138 83 S
Well-BB 10/16/06 289 Well-BB 12/08/06 338 Well-RB 04/10/07
-161 Well-BB 10/17/07
- 149 Well-BR 04/17/08 168 Well-BR 10/20/08
-134 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
,2 toji7 Constituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 86 of 93 1
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample I
Tritium Major Cations and Aniona Identification Date Note Result (pCi/L) I LLD I
Deviation Boron(mg/L)
Sodium(mg/L)
Well-RB 04/13/09 170 137 84 Well-BB 10/21/09 206 135 84 WelI-BC 10/16/06
-163 163 98 Well-BC 04/10/07
,162 162 94-Well-BC 10/17/07
,150 150 89 Well-BC 04/17/08
-144 144 86 Well-BC 04/29/09
.133 133 80 Well-BD 10/16/06 325 157 99 Well-BD 04/10/07 256 152 95 Well-BD 10/10/07 264 156 97 Well-BD 04/22/08 323 148 93 Well-BD 10/20/08 264 133 83 WelI-BD 04/13/09 381 137 88 Well-BD 10/27/09 196 135 84 Well-BE 10/16/06
-159 159 95 Well-BE 04/10/07
-168 168 98 Well-BE 10/10/07
-158 158 93 Well-BE 04/17/08
,152 152 90 Well-BE 10/21/08 659 134 90 Well-BE 04/13/09 449 141 91 Well-BE 06/29/09
,130 130 79 Well-BE 10/27/09 636 1
135 90 Well-BF 10/16/06
'155 155 91 1
Well-BF 04/11/07
-'164 164 94 Well-BF 10/17/07
-'189 189 109 Well-BF 04/17/08
- 152 152 91 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
20 00 Constituent was detected above its New Jersey Groundwater Quality Criteria.
Eitot Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 87 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritiumn Major Cations and Anin Identification Date INote Result (pCiL)I LLD Deviation Boron(mg/L) I Sodinm(mglL)
Well-BF 110/21/08 1
-136 1 36 80-I Well-BF 04/13/09
'141 I
II_41 83 WelI-BF 10/27/09
- 135 135 80 Well-BG 10/17/06 162 162 97 Well-BG 04/11/07
-152 152 92 Well-BG 11/01/07
-165 165 94 Well-BG 04/22/08 322 152 95 Well-BG 10/21/08
-137 137 82 Well-BG 04/29/09 354 143 90 Well-BG 06/15/09 147 133 81 Well-BG 11/19/09 1,591 131 101 Well-BU 04/24/07
-181 181 106 Well-BU 10/18/07
-153 153 90 Well-BU 04/16/08
-157 157 94 Well-BU 10/27/08
'149 149 88 Well-BU 04/16/09
-141 141 86 Well-BU 10/13/09
-141 141 84 Well-BW 02/24/07 2,556 162 132 Well-BW 03/27/07 3,728 164 149 Well-BW 04/20/07 3,054 159 138 Well-BW 05/22/07 1,517 168 122 Well-BW 06/25/07 1
-3,730 3,730 NA Well-BW 07/12/07 1,593 146 110 Well-BW 08/22/07 1,719 149 113 Well-BW 09/21/07 1,917 149 115 Well-BW 10/09/07 2,056 150 117 Well-BW 11/20/07 1,729 179 132 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
266W Constituent was detected above its New Jersey Groundwater Quality Criteria.
ot Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 88 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample ITitium Major Cations and Anions Identification Date Note Result (pCi/L) I LLD Deviation Boron(mg/L)
Sodium(mg/L)
Well-BW 12/19/07 1,641 147 111 WelI-BW 01/16/08 1,638 141 107 Well-BW 02/25/08 1,347 142 104 Well-BW 03/13/08 1,201 138 100 WelI-BW 04/02/08 1,657 151 113 WelI-BW 05/28/08 762 136 93 Well-BW 06/19/08 1,299 135 99 Well-BW 07/08/08 1,569 129 100 Well-BW 08/18/08 1,549 131 101 7
Well-BW 09/22/08 1,915 128 104 Well-BW 10/18/08 1,748 135 106 WelI-BW 11/21/08 1,347 144 105 Well-BW 12/04/08 1,803 146 113 Well-BW 01/19/09 1,224 147 105 Well-BW 02/24/09 1,659 133 103 WelI-BW 03/26/09 1,879 134 106 Well-BW 04/29/09 967 133 94 Well-BW 05/12/09 1,165 138 99 Well-BW 06/08/09 791 133 91 Well-BW 07/16/09 1,343 142 104 Well-BW 08/04/09 609 144 95 Well-BW 09/23/09 853 149 102 Well-BW 10/27/09 713 139 94 Well-BW 11/19/09 538 144 94 Well-BW 12/22/09 450 147 94 Well-BX 02/24/07 1,958 155 120 WelI-BX 03/27/07 962 151 105 Well-BX 04/20/07 883 161 110 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
[
Constituent was detected above its New Jersey Groundwater Quality Criteria.
Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 89 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample ITritium Major Cations and Anions Identification Date Note Result (pCi/L)
LLD I
Deviation Boron(mg/L)
Sodium(mg/L)
Well-BX 05/22/07 1,265 138 102 WelI-BX 06/25/07 1
-3,730 3,730 NA Well-BX 07/12/07 1,556 144 108 Well-BX 08/22/07 1,806 147 113 WelI-BX 09/21/07 1,430 150 110 Well-BX 10/09/07 996 151 104 Well-BX 11/20/07 1,270 173 122 Well-BX 12/19/07 1,378 146 107 Well-BX 01/16/08 1,097 154 107 Well-BX 02/25/08 599 142 94 Well-BX 03/13/08 536 139 91 Well-BX 04/02/08 864 151 103 Well-BX 05/28/08 770 137 93 WelI-BX 06/19/08 1,115 135 97 Well-BX 07/08/08 1,354 129 97 Well-BX 08/18/08 1,189 139 101 Well-BX 09/22/08 3,213 130 120 Well-BX 10/18/08 1,585 149 111 WelI-BX 11/21/08 968 144 100 WelI-BX 12/04/08 1,147 132 96 Well-BX 01/19/09 640 153 100 Well-BX 02/24/09 760 148 100 Well-BX 03/26/09 5,075 127 135 Well-BX 04/29/09 314 143 90 Well-BX 05/12/09 377 139 89 WelI-BX 06/08/09 295 133 84 Well-BX 07/16/09 475 141 91 Well-BX 08/04/09 269 145 91 Well-BX 09/23/09 351 145 92 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
Constituent was detected above its New Jersey Groundwater Quality Criteria.
Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 90 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample ITritiums Major Cations and Anion Identification Date Note Result (pCi/L) I LLD I
Deviation Boron(mg/L)
Sodium(mg/L)
Well-BX 10/27/09 284 140 88' Well-BX 11/19/09 492 132 87 Well-BX 12/22/09 305 146 92 Well-CA 02/21/07 695 161 107 Well-CA 03/15/07 932 165 113 Well-CA 04/11/07 853 160 109 Well-CA 05/22/07 665 170 111 Well-CA 06/19/07 639 138 92 Well-CA 07/12/07 710 144 96 Well-CA 08/22/07 670 147 97 Well-CA 09/20/07 599 150 98 Well-CA 10/09/07 549 153 99 Well-CA 11/19/07 437 177 112 Well-CA 12/19/07 729 146 98 Well-CA 01/16/08 792 156 104 Well-CA 02/20/08 817 141 96 Well-CA 05/28/08 1,006 137 97 Well-CA 06/19/08 992 137 97 Well-CA 07/08/08 964 133 94 Well-CA 08/18/08 647 139 92 Well-CA 09/22/08 753 128 88 Well-CA 10/18/08 568 152 99 Well-CA 11/21/08 1,330 145 106 Well-CA 12/04/08 828 135 93 Well-CA 01/19/09 1,056 134 96 Well-CA 02/24/09 1,077 137 98 Well-CA 03/26/09 1,541 124 96 Well-CA 04/22/09 1,061 141 100 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
[i2-o Constituent was detected above its New Jersey Groundwater Quality Criteria.
NA Not Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 91 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample ITritium Major Cations and Anion Identification Date Note Result (pCiIL) I LLD Deviation Boron(mg/L)
Sodinm(mg/L)
Well-CA 05/12/09 1,164 138 99 Well-CA 06/08/09 977 135 95 Well-CA 07/16/09 868 139 96 Well-CA 08/04/09 730 147 99 Well-CA 09/23/09 526 148 96 Well-CA 11/19/09 814 132 91 Well-CB 02/21/07 156 152 93 Well-CB 03/27/07
-158 158 95 Well-CB 04/11/07
-162 162 97 Well-CB 05/22/07
-180 180 106 Well-CB 06/19/07
-145 145 87 Well-CB 07/12/07
,147 147 89 Well-CB 08/22/07
-149 149 90 Well-CB 09/20/07
-144 144 87 Well-CB 10/09/07
,150 150 89 Well-CB 11/19/07
-180 180 108 Well-CB 12/19/07
-146 146 89 Well-CB 01/16/08
-152 152 91 Well-CB 02/20/08 181 141 87 Well-CB 05/28/08 1,813 137 107 Well-CB 05/29/08 1
'3,730 3,730 NA Well-CB 06/19/08 1,499 143 106 Well-CB 07/08/08 2,730 129 114 Well-CB 08/18/08 1,674 139 107 Well-CB 09/22/08 6,296 146 157 Well-CB 10/18/08 2,074 150 118 Well-CB 11/21/08 1,114 134 97 Well-CB 12/04/08 861 133 92 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
F Constituent was detected above its New Jersey Groundwater Quality Criteria.
N ot Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 92 of 93
Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.
for Samples collected between 01/22/2003 and 12/31/2009 Well Sample Tritium Major Cations and AniTns Identification Date Note Result (pCi/L)
LLD I
Deviation Boron(mg/L)
Sodium(mg/L)
Well-CB 01/19/09 143 133 81 Well-CB 02/24/09 903 137 96 Well-CB 03/26/09 1,551 121 94 Well-CB 04/22/09
-145 145 87 Well-CB 05/12/09 673 145 97 Well-CB 06/08/09 216 129 80 Well-CB 07/16/09 580 142 94 Well-CB 08/04/09 1,493 145 108 Well-CB 09/23/09 221 152 94 Well-CB 11/19/09 289 130 82 Notes:
LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I
Reported analytical results are from Salem Chemistry.
Constituent was not detected above the indicated laboratory detection limit.
762 Constituent was detected above the laboratory method detection limit.
F Constituent was detected above its New Jersey Groundwater Quality Criteria.
ot Available - Deviation and/or LLD were not reported.
Constituent not analyzed.
02/24/2010 11:26 AM Page 93 of 93
Table 03. Unit I Seismic Gap Drain Tritium Analytical Results, PSEG Nuclear, LLC, Salem Generating Station Date of Operation Tritium Results (pCi/L)
October 5, 2004 2,590,000 October 13, 2004 74,600,000 October 21, 2004 75,600,000 October 27, 2004 1,920,000 November 3, 2004 66,300,000 November 8, 2004 103,000,000 November 15, 2004 61,900,000 November 23, 2004 46,800,000 December I, 2004 40,400,000 December 8, 2004 63,400,000 December 14, 2004 44,800,000 December 21, 2004 89,900,000 January 4, 2005 13,600,000 January 1I, 2005 40,900,000 January 19, 2005 17,700,000 January 24, 2005 57,900,000 February 2, 2005 46,700,000 February 9,,2005 53,800,000 February 25, 2005 26,800,000 February 28, 2005 59,400,000 March 9, 2005 31,800,000 March 18, 2005 44,200,000 April 1, 2005 39,300,000 April 13, 2005 34,600,000 April 21, 2005 29,900,000 May II, 2005 25,600,000 May 19, 2005 33,400,000 May 25, 2005 37,400,000 June 9, 2005 35,800,000 July 8, 2005 31,800,000 July 15, 2005 47,900,000 September 4, 2005 32,600,000 September 28, 2005 50,300,000 November 27, 2005 29,700,000 December 26, 2005 27,800,000 February 19, 2006 28,000,000 March 13, 2006 28,000,000 March 20, 2006 28,000,000' March 27, 2006 28,000,000' April 10, 2006 58,400,000 April 17, 2006 70,300,000 April 23,2006 70,300,000 May I, 2006 74,600,000 May 7, 2006 88,000,000 May 14, 2006 85,800,000 May 20, 2006 83,800,000 May 27, 2006 6,970,000 May 29, 2006 ND June 5, 2006 ND June 12, 2006 73,100,000 June 18, 2006 58,400,000 June 25, 2006 72,400,000 June 29, 2006 63,200,000 Jul 2, 2006 30,000,000 July 15, 2006 30,000,000 July 22, 2006 63,200,000 July 29, 2006 36,300,000 August 5, 2006 45,800,000 August 12, 2006 68,600,000 August 20, 2006 68,600,000 September 17, 2006 123,000,000 September 30, 2006 118,000,000 October 7, 2006 128,000,000 October 14, 2006 133,000,000 October 21, 2006 116,000,000 October 28, 2006 84,000,000 November 4, 2006 113,000,000 November II, 2006 100,000,000 Notes:
concentration estimated based upon results of prior events ND = Data not availible Volume data after September 2005 estimated due to change in draining proceedures.
Date of Operation Tritium Results (pCi/L)
November 19, 2006 97,200,000 November 25, 2006 116,000,000 December 2, 2006 122,000,000 December 9, 2006 110,000,000 December 17, 2006 100,000,000 December 23, 2006 115,000,000 December 31, 2006 134,000,000 January 8, 2007 131,000,000 January 14, 2007 105,000,000 January 21, 2007 102,000,000 January 27, 2007 77,900,000 February 3, 2007 71,800,000 February I1, 2007 67,700,000 February 17, 2007 67,400,000 February 24, 2007 66,400,000 March 3, 2007 76,000,000 March 7, 2007 40,800,000 March 25, 2007 75,800,000 April 15, 2007 69,900,000 April 20, 2007 1,770,000 May I, 2007 58,600,000 May 6, 2007 79,100,000 May II, 2007 80,900,000 May 13, 2007 77,100,000 May 15, 2007 82,300,000 May 16, 2007 82,600,000 May 18, 2007 82,900,000 June I, 2007 65,700,000 June 10, 2007 66,600,000 June 17, 2007 63,200,000 June 21, 2007 70,200,000 June 24, 2007 73,900,000 June 26, 2007 81,400,000 July 6, 2007 39,000,000 July 8, 2007 1,970,000 July 1I, 2007 66,200,000 July 19, 2007 60,400,000 July 24, 2007 57,300,000 July 29, 2007 12,800,000 August 5, 2007 61,500,000 August 12, 2007 66,600,000 August 15, 2007 71,400,000 August 21, 2007 76,400,000 August 26, 2007 66,300,000 September 6, 2007 88,200,000 September 9, 2007 87,000,000 September 16, 2007 89,000,000 September 26, 2007 100,000,000 October 7, 2007 94,600,000 October 14, 2007 98,200,000 October 21, 2007 190,000,000 October 24, 2007 107,000,000 November I, 2007 100,000,000 November 4, 2007 97,400,000 November II, 2007 102,000,000 November 19, 2007 4,800,000 November 30, 2007 99,000,000 December 9, 2007 124,000,000 December 16, 2007 107,000,000 December 23, 2007 40,500,000 January 6, 2008 107,000,000 January 13, 2008 70,900,000 January 20, 2008 104,000,000 Januray 27, 2008 ND February 3, 2008 139,000,000 February 10, 2008 509,000 February 17, 2008 ND February 20, 2008 144,000,000 1 of 2
Table 03 Unit I Seismic Gap Drain Tritium Analytical Results, PSEG Nuclear, LLC, Salem Generating Station Date of Operation Tritium Results (pCi/L)
Date of Operation Tritium Results (pCi/L)
February 24, 2008 142,000,000 March 2, 2008 149,000,000 March 9, 2008 142,000,000 March 16, 2008 169,000,000 March 23, 2008 178,000,000 March 30, 2008 164,000,000 April 6, 2008 181,000,000 April 13, 2008 170,000,000 April 20, 2008 183,000,000 April 27, 2008 5,860,000 May 4, 2008 169,000,000 May 11, 2008 159,000,000 May 19, 2008 154,000,000 May 25, 2008 82,000,000 June 1, 2008 145,000,000 June 10, 2008 150,000,000 June 15, 2008 I 10,000,000 June 22, 2008 168,000,000 June 29, 2008 191,000,000 July 6, 2008 23 1,000,000 July 13, 2008 ND July 20, 2008 212,000,000 July 27, 2008 212,000,000 August 3, 2008 209,000,000 August 10, 2008 165,000,000 August 16, 2008 221,000,000 August 24, 2008 229,000,000 August 31, 2008 246,000,000 September 7, 2008 ND September 14, 2008 250,000,000 September 21, 2008 246,000,000 September 28, 2008 ND October 5, 2008 ND October 12, 2008 ND October 19, 2008 ND October 27, 2008 200,000,000 November 2, 2008 238,000,000 November 9, 2008 ND November 23, 2008 ND November 30, 2008 ND December 6, 2008 172,000,000 December 14, 2008 186,000,000 December 21, 2008 181,000,000 December 27, 2008 202,000,000 January 4, 2009 143,000,000 January 1I, 2009 166,000,000 January 17, 2009 164,000,000 January 25, 2009 171,000,000 February 1,2009 172,000,000 February 8, 2009 N D February 10, 2009 163,000,000 February 15, 2009 160,000,000 February 22, 2009 176,000,000 March I, 2009 184,000,000 March 8, 2009 168,000,000 March 14, 2009 190,000,000 March 22, 2009 189,000,000 March 30, 2009 188,000,000 April 4, 2009 200,000,000 April 12, 2009 190,000,000 April 19,2009 180,000,000 April 26, 2009 168,000,000 May 2, 2009 5,980,000 May 10, 2009 166,000,000 May 17, 2009 165,000,000 May 24, 2009 143,000,000 May 31, 2009 164,000,000 June 7, 2009 176,000,000 June 14, 2009 167,000,000 Notes:
' concentration estimated based upon results of prior events ND = Data not availible Volume data after September 2005 estimated due to change in draining proceedures.
Date of Operation Tritium Results (pCi/L)
Date of Operation Tritium Results (pCi/L)
June 20, 2009 151,000,000 June 28, 2009 124,000,000 July 5, 2009 167,000,000 July 12, 2009 189,000,000 July 19,2009 218,000,000 July 25, 2009 91,400,000 August 2, 2009 22,600,000 August 9, 2009 62,100,000 August 16, 2009 50,000,000 August 23,'2009 21,500,000 August 30, 2009 45,800,000 September 5, 2009 73,800,000 September 13, 2009 56,400,000 September 19, 2009 79,000,000 September 27, 2009 87,600,000 October 4, 2009 98,900,000 October 12, 2009 98,000,000 October 18, 2009 76,500,000 October 25, 2009 135,000,000 November 1, 2009 115,000,000 November 8, 2009 147,000,000 November 15, 2009 147,000,000 November 22, 2009 164,000,000 November 29, 2009 156,000,000 December 5, 2009 158,000,000 December 13, 2009 748,000 December 20, 2009 142,000,000 December 26, 2009 48,200,000 2 of 2
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