ML20023D976

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IE Insp Rept 50-334/83-08 on 830405-0502.Noncompliance Noted:Failure to Demonstrate ECCS Valve Operability within Specified Surveillance Interval
ML20023D976
Person / Time
Site: Beaver Valley
Issue date: 05/17/1983
From: Lester Tripp, Troskoski W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20023D959 List:
References
RTR-NUREG-0737, RTR-NUREG-737, TASK-1.C.6, TASK-TM 50-334-83-08, 50-334-83-8, IEB-82-01, IEB-82-02, IEB-82-03, IEB-82-04, IEB-82-1, IEB-82-2, IEB-82-3, IEB-82-4, IEB-83-02, IEB-83-04, IEB-83-2, IEB-83-4, NUDOCS 8306060214
Download: ML20023D976 (22)


See also: IR 05000334/1983008

Text

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U. S. NUCLEAR REGULATORY CO MISSION

REGION 1

Report No.

50-334/83-08

Docket No.

50-334

License No.

DPR-66

Priority

Category

C

--

Licensee:

Duquesne Light Company

435 Sixth Avenue

Pittsburgh, Pennsylvania

,

Facility Name:

Beaver Valley Power Station, Unit 1

Inspection at:

Shippingport, Pennsylvania

Inspection Conducted: April 5 - May 2,1983

Inspector:

5

. 4@/)

7

3

. M. Tro&Koski, Resident Inspector

date signed

/

Approved by:

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73

L. E. Tripp, Chief, Reactor Projects

date signed

Section No. 2A, Reactor Projects

Branch 2

Inspection Summary:

Inspection an April 5 - May 2,1983 (Inspection No.

50-334/83-08).

Areas Inspected:

Routine inspections by the resident inspector (100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br />) of:

licensee action on previous inspection findings, plant operations, housekeeping,

fire protection, radiological controls, physical security, maintenance

activities, surveillance testing, engineered safety features verification,

refueling preparation, radioactive waste transportation activities, safety

and quality classification of equipment, changes, tests and experiments

program, and IE Bulletins.

Results: One violation (failure to demonstrate ECCS valve operability

within specified surveillance interval - detail 5).

8306060214 830523

PDR ADOCK 05000334

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DCS NUMBERS

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821229

821014

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810519

821028

800822

821203

830322

830304

830328

830311

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820331

830329

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DETAILS

1.

Persons Contacted

F. Bissert, Manager, Nuclear Support Services

J. Carey, Vice President, Nuclear Division

M. Coppula, Superintendent of Technical Services

K. Grada, Superintendent of Licensing and Compliance

R. Hansen, Maintenance Supervisor

J. Indovina, I&C Supervisor

T. Jones, Manager, Nuclear Operations

J. Kosmal, Radiological Operations Coordinator

W. Lacey, Station Superintendent

V. Linnenbom, Radiochemist

J. Lukehart, Security Director

L. Schad, Operations Supervisor

E. Schnell, Radcon Supervisor

J. Sieber, Manager, Nuclear Safety and Licensing

R. Swiderski, Superintendent of Nuclear Construction

N. Tonet, Manager, Nuclear Engineering

T. Zyra, Plant Performance and Testing Supervisor

The inspector also contacted other licensee employees and contractors

during this inspection.

2.

The NRC Outstanding Items (0I) List was reviewed with cognizant licensee

personnel.

Items selected by the inspector were subsequently reviewed

through discussions with licensee personnel, documentation review and

field inspection to detennine whether licensee actions specified in

the OIs had been satisfactorily completed. The overall status of

previously identified inspection findings were reviewed, and planned

and completed licensee actions were discussed for those items reported

below.

(Closed) Violation (82-25-03): Failure to review and approve tank curve

notebook. By response dated December 29, 1982, DLC committed to review

the accuracy of the reference curves of tanks used for liquid waste

discharges and surveillance testing, and to submit the entire curve book

to the Onsite Safety Conmittee for review and subsequent approval by the

Station Superintendent. The inspector reviewed the control room tank

curve book and verified that it was approved and controlled per OM

Chapter 1.48.9, Procedure M, Revisions or Reissues to Operating Manual

Flow Diagrams. This item is closed.

1

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(Closed)UnresolvedItem(81-04-01):

Review DLC evaluation of PAB

ventilation system perfomance. This item was to provide further

review of a November 25, 1980 event (discussed in NRC Inspection Report

No. 50-334/80-30) where the maximum pemissible concentration of Xenon

and various daughter products in a restricted area was detemined to

be about 28%, due to primary leakage from the reactor coolant system

filter. Completion of corrective actions to insure design performance

of the PAB ventilation system were documented in that inspection report.

In addition to those items, the licensee rebalanced PAB ventilation

system and attempted to correlate any higher than normal background

radiation / airborne radioactivity levels to specific plant evolutions.

Preliminary infomation was assembled by the Radcon staff and forwarded

to Operations for identification of process evolutions occuring during

the same time period. No meaningful correlation could be obtained.

During the course of 1983, the inspector observed several instances

where Xenon and various decay products were detected in the PAB.

In

each case, the maximum concentrations were significantly below MPC

limits. Because those particular isotopes decay to background levels

in approximately 30 minutes and no radiological safety concern is present,

this item is closed.

(Closed) Unresolved Item (81-29-01): Bases for 10 CFR 50.59 procedure

reviews not documented by OSC. The inspector reviewed the Onsite

Safety Committee meeting minutes of 1983 and verified that written

evaluations of new procedures, or changes to existing procedures, were

provided per the provisions of 10 CFR 50.59 that detail the bases for

detemining that no unreviewed safety question is involved. Administrative

chaages to procedures that did not affect the intent were so identified

on a generic basis. Those written evaluations now allow the Offsite

Review Committee to better perform their subsequent TS 6.5.2.7 required

reviews. This item is closed.

(Closed) Unresolved Item (80-24-01):

Inadequate review of design changes

by OSC for technical specification impact. Various design change packages

and associated safety analysis were reviewed and accepted by the OSC

without properly identifying technical specification changes needing prior

Commission approval. Subsequent inspection of this area indicated that

the design concepts continued to evolve after the preliminary safety

evaluation was perfomed; some to the point where they impacted on the

technical specifications. To correct this program deficiency, the

licensee revised Station Engineering Procedure 2.3, Design Change

Coordination, to require a new safety evaluation on any design concept

that is substantially changed after the initial review. The new safety

evaluation is then forwarded to the OSC for their review and approval.

The inspector reviewed a sampling of DCPs performed in 1982 to verify

proper program implementation. Additionally, the licensee has performed

a systematic review of all pre-refueling Category 1 design changes per

the revised SEP 2.3 criteria (as detailed in Unresolved Item 80-09-14

and discussed in this report section). This item is now closed.

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(Closed)UnresolvedItem(80-09-14): DLC to access quality of as-built

infomation. To access the quality and accuracy of station drawings,

procedures, and engineering infomation, the licensee perfomed a

systematic review of all pre-refueling Category 1 design changes. This

,

review was conducted per Station Engineering Procedure 2.3, Design

!

Change Coordination, which identifies and assigns responsibility for

!

various turnover activities to applicable station groups. The inspector

reviewed selected DCPs referenced in the Engineering Matrix Program

and confimed that the reviews (including TS, SAR, and 10 CFR 50.59)

were conducted between March and July,1981. This item is closed.

(Closed) Unresolved Item (80-24-02): Adequate content of bases used

for unreviewed safety questions. A previous inspector concern questioned

the adequacy of the documented basis provided for the 10 CFR 50.59 review

of several design change packages. The licensee infomed the inspector

that in the future, guidance provided by IE Circular 80-18, Safety Evaluations

!

for Changes to Radioactive Waste Treatment Systems, would be employed

during the preparation of all. bases used to detemine whether or not the

design change involved an unreviewed safety question. Both SEP 2.3, for

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the Station Engineering Group and NEMP 2.3, for the Nuclear Engineering

Division, were revised to provide this guidance for evaluating each

proposed station modification. This item is closed.

~

(Closed)UnresolvedItem(82-11-01): Technical Specification Table 3.6 - 1

to be updated to reflect modifications to the containment system boundries.

!

During containment local leak rate testing conducted during May,1982, the

inspector noted that several plant modifications necessitated a change to

'

TS Table 3.6-1. Containment Penetrations. TS Amendment No. 65 approved

March 22, 1983, waives the need for Type C testing of certain valves that

do not represent potential containment atmosphere leakage paths, and

therefore, are not subject to 10 CFR 50, Appendix J, Section C require-

ments. This item is closed.

'

3.

Plant Operations

!

a.

General

l

Inspection tours of the plant areas listed below were conducted

during both day and night shifts with respect to Technical Spec-

ification (TS) compliance, housekeeping and cleanliness, fire

protection, radiation control, physical security and plant pro-

.

tection, operational and maintenance administrative controls.

Control Room

--

-- Primary Auxiliary Building

Turbine Building

--

Service Building

--

-- Main Intake Structure

Main Steam Valve Room

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Purge Duct Room

--

East / West Cable Vaults

--

-- Emergency Diesel Generator Rooms

Containment Building

--

Penetration Areas

--

Safeguards Areas

--

Various Switchgear Rooms / Cable Spreading Room

--

Protected Areas

--

Acceptance criteria for the above areas include the following:

BVPS FSAR Appendix A, Technical Specifications (TS)

--

-- BVPS Operating Manual (0M), Chapter 48, Conduct of Operations

OM 1.48.5, Section D, Jumpers and Lifted Leads

--

OM 1.48.6, Clearance Procedures

--

OM l.48.8, Records

--

OM 1.48.9, Rules of Practice

--

-- OM Chapter 55A, Periodic Checks - Operating Surveillance Tests

BVPS Maintenance Manual (MM), Chapter 1, Conduct of Maintenance

--

-- BVPS Radcon Manual (RCM)

10 CFR 50.54 (k), Control Room Manning Requirements

--

-- BVPS Site / Station Administrative Procedures (SAP)

BVPS Physical Security Plan (PSP)

--

Inspector Judgement

--

b.

Operations

The inspector toured the Control Room regularly to verify compliance

with NRC requirements and facility technical specifications (TS).

Direct observations of instrumentation, recorder traces and control

panels were made for items important to safety.

Included in the

reviews are the rod position indicators, nuclear instrumentation

systems, radiation monitors, containment pressure and temperature

parameters, onsite/offsite emergency power sources, availability

i

of reactor protection systems and proper alignment of engineered

safety feature systems. Where an abnormal condition existed (such

as out-of-service equipment), adherence to appropriate TS action

statements were independently verified. Also, various operation

logs and records, including completed surveillance tests, equip-

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ment clearance permits in progress, status board maintenance and

temporary operating procedures were reviewed en a sampling bases

for compliance with technical specifications and those administrative

controls listed in paragraph 3a.

During the course of the inspection, discussions were conducted

with operators concerning reasons for selected annunciators and

knowledge of recent changes to procedures, facility configuration

,

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and plant conditions. The inspector verified adherence to approved

procedures for ongoing activities observed. Shift turnovers were

witnessed and staffing requirements confirmed. Except as noted

below, inspector comments or questions resulting from these daily

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reviews were acceptably resolved by licensee personnel.

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(1) During perfomance of OST 1.1.11, Safeguards Protection

System Train A Test, on April 11, 1983, safety injection

transfer relay K 641, failed a contact continuity check.

Investigation indicated that M0V-SI860A (low head SI pump

suction valve from containment) themal overload had tripped.

The themal overload relay was checked and Preventive

Maintenance Procedure 1-75-MOV-lE was performed on the

valve breaker, but the problem could not be duplicated.

The OST was reperformed satisfactorily and the system

declared operable.

A review of the equipment history

list did not identify any similar failures. The inspector

had no further concerns.

(2) From about April 10th to 17th, 1983, the containment sump

pump-out rate (as indicated on FTO-DA-102) increased from

about 1 gallon per minute to approximately 2 gallons per

minute. The licensee conducted a containment entry on

April 16, 1983, to identify the source of increased in-

leakage. The suspected leak path was identified as coming

from valve packing on a manual isolation valve (80-14) in

the steam generator blowdown line at the B cubicle 738'

elevation. This leakage was in the fom of steam from the

secondary side and did not present a radiological hazard

as indicated by no measured increase in containment parti-

culate or gaseous activity. The licensee informed the

inspector that another containment entry was planned in

an attempt to Furmanite the valve packing. The inspector

discussed licensee plans for maintaining exposures during

this job to levels that are as low as reasonably achievable

(ALARA). Radiation Work Permit 11008 and associated documentation

were reviewed to verify that proper containment air sampling

was made to calculate the maximum pemissible concentration

(MPC) hours, that exposure limits were properly reviewed and

authorized and that contractor personnel were properly rad-

worker qualified. Pocket dt.,imetry records indicated that

the total man-Rem exposure for the job was approximately

1.4 R.

When comparing this data to the initial pre-job

survey of the area which indicated a 5 to 7 R field, the

licensee's pre-planning efforts were effective in minimizing

total exposure. No individual

exceeded the DLC administrative

guidelines. Additionally, the results of the maintenance

efforts were successful in reducing the secondary leakage

rate back down to about 60 gallons per hour.

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(3) On April 21, 1983, it was detennined that 26 of 50 axial

flux thimbles were blocked. Technical Specification 3.3.3.2, Moveable Incore Detectors, requires that at least

50% of the detector paths are passable, whenever the system

is used to:

(1) recalibrate the axial flux offset system;

(2) monit'.,r the quadrant power tilt ratio; or, (3) to measure

the Nuclear Enthalpy and Heat Flux hot channel factors.

Through discussicns with the reactor engineer, the inspector

detennined that the next required hot channel factor measure-

ments and recalibration of the axial flux offset detector

system would be due on May 16, 1983. Monitoring of the

quadrant power tilt ratio by this system is not necessary

as all four power range nuclear instruments are operable.

This item will receive continued attention.

(4) At about 4:45 a.m. on April 29, 1983, boronometer relief

valve RV-CH-103 (located down stream on the nonregenerative

heat exchanger in the 722' elevation of the PAB) lifted,

releasing a small amount of RCS water to the PAB sump that

off-gased an estimated 3.8 curies of Noble gas (Xe-133).

No iodines were detected and maximum particulates (Rb-88,

Cs-138) were 8 E-8 microcuries per cc.

PAB ventilation

monitors increased about 250 counts per minute above back-

ground before tailing off to normal levels at 8:00 a.m.

There was no spread of contamination and gas samples

indicated less than minimum detectible activity (about 3.6

E-8 microcuries per cc).

The inspector reviewed the various

gas samples taken during the event. Calculations indicated

that the gaseous release was less than 1.5% of the

instantaneoas technical specification values and less than

1.7% for skin dose.

Regional NRC health physics specialists

had no further radiological concerns about this event.

During this event, the licensee was performing two compatable

evaluations in parallel; an RCS inventory calculation per

OST 1.6.2, and an RCS dilution to maintain T-average. This

involved filling the volume control tank (VCT) to its upper

level with primary makeup water and isolating the degasifier

flow path. Total head on the boronometer (recently unisolated

for corrective maintenance) was estimated to be no more than

65 psi when RV-CH-103 lifted

(normal lift point should have

been 200 psi), setting off PAB radiation monitors. The boron-

ometer was reisolated to prevent RV-CH-103 from failing again.

Appropriate NRC notifications were made via the ENS system.

Licensee actions were satisfactory.

_ . _

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c.

Plant Security / Physical Protection

Implementation of the Physical Security Plan was observed in the

areas listed in paragraph 3a above with regard to the following:

Protected area barriers were not degraded;

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Isolation zones were clear;

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Persons and packages were checked prior to allowing entry

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into the Protected Area;

Vehicles were properly searched and vehicle access to the

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Protected Areas was in accordance with approved procedures;

Security access controls to Vital Areas were being maintained

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and that persons in Vital Areas were properly authorized;

Security posts were adequately manned, equipped and security

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personnel were alert and knowledgeable regarding position

requirements, and that written procedures were available; and,

-- Adequate lighting maintained.

The inspector identified no deficiencies.

d.

Radiation Controls

Radiation controls, including posting of radiation areas, the

conditions of step-off pads, disposal of protective clothing,

completion of Radiation Work Permits, compliance with Radiation

Work Pennits, personnel monitoring devices being worn, clean-

liness of work areas, radiation control job coverage, area monitor

operability (portable and pennanent), area monitor calibration,

and personnel frisking procedures were observed on a sampling basis.

No violations were identified.

e.

Plant Housekeeping and Fire Protection

Plant % sekeeping conditions including general cleanliness

conditions and control of material to prevent fire hazards were

observed in areas listed in paragraph 3a. Maintenance of fire

barriers, fire barrier penetrations, and verification of posted

fire watches in these areas was also observed. No inadequacies

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were observed.

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f,

Chemistry Sampling Program

The inspector reviewed DLC's chemistry log sheets for technical

specification required sampling of the reactor coolant system

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chemistry (dissolved oxygen, chloride, fluoride), gross activity,

,

and dose equivalent Iodine - 131 for the period of April 1 - 25,

,

1983. Additionally, boric acid sampling logs of the BIT, RWST,

SI accumulators, and boric acid storage tanks were also audited

for~that time period. From this review, it was determined that

the licensee's sampling program was being properly implemented

per applicable technical specification requirements and that the

sampling frequency and individual parameters were within limits.

No discrepancies were noted.

g.

Liquid Waste Discharges

,

References:

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1.

Updated FSAR, Section ll, Radioactive Waste and Radiation

Protection.

2.

Regulatory Guide 1.21, Measuring, Evaluating and Reporting

Radioactivity in Solid Wastes and Releases of Radioactive

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Material in Liquid and Gaseous Effluents from Light Water

Cooled Nuclear Power Plants.

3.

BVPS Technical Specification Amendment No. 66.

!

4.

10 CFR 50 Appendix I, Numerical Guides for Design Objectives

in Limiting Conditions for Operations to meet the Criterion

"As Low As is Reasonably Achievable" for Radioactive Material

in Light Water Cooled Nuclear Power Effluents.

5.

Operating Manual, Chapter 1.17, Liquid Waste Disposal System.

Amendment No. 66 to the BVPS Technical Specifications updates the

radiological effluent technical specifications that are outlined

,

in the ETS. This amendment is effective as of March 28,1983, and

,

'

is scheduled to be fully phased in by January 1, 1984.

It imple-

ments the requirements of Appendix I to 10 CFR 50 and establishes

new limiting conditions for operation for the quarterly and annual

average release rate and revises environmental monitoring programs

to assure conformance with Commission regulations. The inspector

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conducted discussions with cognizant licensee representatives on

phasing in the various aspects of the new RETS program, in particular,

i

with respect to the Offsite Dose Calculation Manual and the radioactive

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waste discharge program. Responsibilities and authorities have

'

already been assigned in this regard to meet the January 1,1984,

,

deadline. This item will receive further review as the program

progresses.

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The duty on the liquid waste system was increased due to the higher

than nomal containment sump pirip-out rate (130-140 gallons per

hour) in April. The inspector reviewed liquid radioactive waste

discharge authorization (RWDA) Numbers 2220 to 2253 to verify

chemistry limits on chromates, minimum dilution flows, proper

recirculation time prior to sampling, rad monitor alarm setpoint

calculations, isotopic sampling and recording, and proper reviews

and approvals from the Operations, Radcon and Chemistry Departments

were obtained per the above administrative guidelines. The inspector

also reviewed the requirements of Regulatory Guide 1.21 to verify

that they were properly translated into the Operating Manual

Chapter 17 Procedures. Licensee actions were found to be consistent

with those requirements.

4.

Engineered Safety Features (ESF) Verification

A.

The operability of the low head safety injection, chemical addition,

containment depressurization and cooling systems were verified by

performing a walkdown of accessible portions that included the

following as appropriate:

1.

System lineup procedures match plant drawings and the as-

built configuration.

2.

Equipment conditions were observed for items which might

degrade perfomance. Hangers and supports are operable.

3.

The interior of breakers, electrical and instrumentation

cabinets were inspected for debris, loose material, jumpers,

etc.

4.

Instrumentation was properly valved in and functioning; and

had current calibration dates.

5.

Valves were verified to be in the proper position with power

available. Valve locking mechanisms were checked, where

required.

6.

Technical Specification required surveillance testing was

current.

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Findings:

(1) Technical Specification 4.6.2.3 requires that each valve (manual,

power operated, or automatic) in the chemical addition flow path

that is not locked, sealed or otherwise secured in position, be

checked for correct alignment on a 31 day frequency. A review

of OSTs related to OM Chapter 13, Containment Depressurization

System, and the Pad Lock log book indicated that manual valve

QS-186 (the manual isolation valve to the chemical addition

tank, QS-TK-2) was not listed as being checked on a 31 day

frequency. Through discussions with the Operations Supervisor,

the licensee was able to demonstrate correct alignment by virtue

of running OST 1.13.10A(B), Chemical Addition System Valve

Position and Pump Operability Check - Train A(B), on a monthly

frequency (staggered every other week between ESF trains).

NUREG-0737, Clarification of TMI Action Plan Requirements Section

I.C.6, Guidance on Procedures for Verifying Correct Performance

of Operating Activities, provides guidance for the return to service

of equipment important to safety that includes proper system align-

ment verification by second qualified operator or perfomance of

a functional test which can prove that all equipment, valves and

switches involved are correctly ali

Because line flow is

fully demonstrated by OST 1.13.10A(gned.B),theinspectordetermined

that the licensee is in compliance with the surveillance require-

ment, and has no further questions on this item.

(2) During perfomance of a low head safety injection system walkdown

on April 22, 1983, the inspector entered the Safeguards Valvc Pit

and noted that M0V-SI862 A and B, (low head SI pump suction valves

from the RWST) had boric acid buildup on the valve bolts. The

inspector brought this to the licensee's attention and reviewed

station efforts to identify, evaluate and clean up boric acid

buildup on safety related valves and equipment.

For the primary reactor coolant system, residual heat removal

system and portions of the safety injection system located inside

containment, IE Bulletin 82-02 specifies required actions to be

undertaken by the licensee during the upcoming refueling outage

scheduled for June,1983 (see detail 8 of this inspection report).

To assure that high energy ECCS lines and associated boundries

outside of containment do not degrade, a quarterly walkdown is

performed per OST 1.48.2, High Energy Line and ECCS Inspection

(last completed March 26, 1983).

Identified deficier.:ies are

corrected per the maintenance work request system. Additionally,

QC is scheduled to perform an ASME Code Section XI inspection

during the planned June outage. The scope and content of these

inspections are currently being reviewed by the inspector.

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5.

Surveillance Activities

To ascertain that surveillance of safety-related systems or components

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is being conducted in accordance with license requirements, the

inspector observed portions of selected tests to verify that:

a.

The surveillance test procedure confoms to technical

specification requirements.

b.

Required administrative approvals and tagouts are obtained

before initiating the teste

c.

Testing is being accomplished by qualified personnel in

accordance with an approved test procedure.

d.

Required test instrumentation is calibrated.

e.

LCOs are met.

f.

The test data are accurate and comnlete. Selected test

result data was independently reviewed to verify accuracy.

g.

Independently verify the system was properly returned to

service.

h.

Test results meet technical specification requirements and

test discrepancies are rectified.

i. The surveillance test was completed at the required frequency.

OST 1.13.2,1B Quench Spray Pump Flow Test, perfomed

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April 6,1983.

OST 1.11.6, ECCS Flow Path and Valve Position Check

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(LHSI Loop A), perfomed April 21, 1983.

OST 1.13.10B, Chemical Addition System Valve Position and

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Pump Operability Check - Train B, performed April 26, 1983.

MSP 2.09, Nuclear Instrument Source Range Calibration,

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perfomed May 2,1933.

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Findings:

(1) The cover sheet of OST 1.11.6 references TSs 4.5.2.b.3, 4, 5

and 4.5.3 for demonstrating operability of the ECCS. TS 4.5.2.b.5 requires the licensee to verify that each ECCS sub-

system is aligned to receive electrical power from separate

operable emergency buses; yet the purpose of OST 1.11.6 is only

to exercise specified valves and verify their correct position.

Electrical bus alignments are checked per OM Chapter 36

surveillance tests. DLC is currently reviewing procedures that

perfom TS surveillance requirements to verify proper review and

approval. This is being tracked as unresolved item 83-07-04 and

should result in the development of a matrix that cross-references

each surveillance requirement with an appropriate procedure.

Verification that the OST cover sheets accurately reflect

actual TS surveillance requirements tested is an unresolved item

(83-08-01).

(2) The inspector had previously reviewed Section 6, Engineered Safety

Features, of the Updated FSAR, OM Chapter 11 and related OSTs, and

P&ID No. 8600-RM-167A as part of the low head safety injection

system walkdown. During perfomance of OST 1.11.6, it was noted

that MOV-SI 862 A and B, the low head SI pump suction valves

from the RWST, were not being cycled on a 31 day frequency as

required by TS 4.5.2.b.3, but on a quarterly basis as part of

the inservice inspection program per OST 1.47.3A, Three Month

Containment Isolation and ASME Section XI Tests. These valves

would be required to automatically close during changeover to

the recirculation phase of a safety injection. Failure to cycle

each testable power operated valve in the ECCS flow path on a

31 day frequency is a Violation (83-08-02) of TS 4.5.2.b.3.

6.

Maintenance Activities

The inspector observed portions of selected maintenance activities on

safety-related systems and components to verify that those activities

were being conducted in accordance with approved procedures, technical

specifications and appropriate industrial codes and standards. The

inspector conducted record reviews and direct observations to determine

that:

- Those activities did not violate a limiting condition

for operation.

- Redundant components were operable.

- Required administrative approvals and tagouts had been

obtained prior to initiating work.

- Approved procedures were used or the activity was within

the " skills of the trade."

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- The work was performed by qualified personnel.

- The procedures used were adequate to control the activity.

- Replacement parts and materials were properly certified.

- Radiological controls were properly implemented when necessary.

- Ignition / fire prevention controls were appropriate for the

activity.

- QC hold points were established where required and observed.

- Equipment was properly tested before being returned to service.

- An independent verification was conducted to verify that the

equipment was properly returned to service.

(1) Continued repa'r/rebuildir

f river u ter pump WR-P-1A

per MWR 807135.

7.

Refueling Preparation

>

The inspector reviewed DLC quak ty assurance audits, BV-1-82-41, 83-03,

and 83-17, that evaluated the Wstinghouse Nuclear Fuel' Division's

compliance with those requiremeats contained in the DLC QA Nuclear

Fuel Program and Westinghouse WCAP 7800, Nuclear Fuel Quality Assurance

Program. These onsite audits covered fuel pellet manufacturing,

vendor qualifications, design controls, testing, inspection, account-

ability and shipping, and fulfill DLC's obligation to conduct onsite

inspection of the nuclear fuel vendor.

8.

IE Bulletins

Licensee actions on IE Bulletins issued in 1982 and 1983 were inspected

to verify that they were reviewed by licensee management for applicability,

and appropriate corrective actions were taken or scheduled for those

items pertaining to BVPS, as specified in Nuclear Division Directive

No.13, Administration of NRC Bulletins, Circulars and Information Notices.

1.

IEB 82-01:

Rev. 1, Alteration of Radiographs of Welds in Piping

Subassemblies. This bulletin was received by the licensing and

compliance group and forwarded to the Quality Assurance and Quality

Control Departments for general information and review by cognizant

personnel in documented training sessions. This bulletin is closed.

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2.

IEB 82-03: Stress Corrosion Cracking in Thick-Wall, Large-

Diameter Stainless Steel, Recirculation System Piping .

at BWR Plants. This bulletin pertaining to operating boiling

water reactors, was forwarded to DLC for information only.

Cognizant licensee personnel received and reviewed this bulletin.

3.

IEB 82-04:

Deficiencies in Primary Containment Electrical

Penetration Assemblies. Review by the Nuclear Engineering Division,

documented in EM 30214, January 10, 1983, and field observations by

the inspector, detennined that no Bunko Ramo primary containment

electrical penetration assemblies are used at BVPS (Viking assemblies

are employed). This IE Bulletin was added to the engineering equip-

ment qualification file by the licensee for future reference on

possible procurement and installation of the subject assemblies.

This bulletin is closed.

4.

IEB 83-02:

Stress Corrosion Cracking in Large-Diameter Stainless

Steel Recirculation System Piping at BWR Plants. This is an

infonnation type bulletin not directly applicable to the Beaver

Valley Power Station, that was reviewed for information purposes

only.

5.

IEB 83-04: Failure of Undervoltage Trip Function of Reactor Trip

Breakers. This bulletin is not applicable to Beaver Valley Power

Station Unit #1 as Westinghouse Model DB-50 type breakers are usedin

the reactor protection system. Licensee actions on this generic

problem are governed by IEB 83-01, which was inspected in NRC

Inspection Report No. 50-334/83-04,

6.

IEB 82-02:

Degradation of Threaded Fasteners in the Reactor

Coolant Pressure Boundry of PWR Plants. This bulletin was issued

to notify all PWR reactor facilities about severe degracation of

threaded fasteners (bolts and studs) encountered in the reactor

coolant pressure boundry and to require appropriate action.

Included

were steam generator and pressurizer manway covers, valve bonnets,

pump flange connections installed on lines having a nominal diameter

of 6" or greater, and control rod drive flange and pressurizer

heater connections that do not have sealed welds to provide leak

tight intregrity. The inspector reviewed the licensee's response

to this bulletin dated August 2, :982, and could not determine

whether the control rod drive flang3 and pressurizer heater

connections were seal-welded (0mega seal

weld design) and therefore,

excluded from this bulletin action, or whether DLC is connitted to

Reg Guide 1.65, Materials and Inspection for Reactor Vessel Closure

Studs, which would negate further action on the vessel head studs.

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Thisitemisunresolved(83-08-03) pending such detennination.

The inspector verified through review of the reactor coolant

system, residual heat removal system, and safety injection system

prints and diagrams that the remainder of the licensee's planned

inspection scope, as contained in Engineering Memorandum 30165,

meets the intent of the bulletin. The inspector also determined

that those threaded fasteners and closure connections identified

in the EM are scheduled to be opened for component inspection or

maintenance during the next refueling outage scheduled for mid-

June, 1983. This bulletin remains open pending completion of

those actions.

9.

Changes, Tests and Experiments

10 CFR 50.59, Changes, Tests and Experiments, allows the licensee

to make changes in the facility and procedures as described in the

Safety Analysis Report (SAR) and to conduct tests or experiments not

described in the SAR without prior Commission approval unless it involves

a change to the Technical Specifications or an unreviewed safety

question. The DLC program that controls such changes, tests and

experiments was inspected to insure that an adequate 10 CFR 50.59

review is conducted in accordance with established administrative

controls. These controls were also reviewed to verify that:

(1)

a formal method had been established to handle requests or proposals

for conducting plant tests and experiments involving safety related

equipment or modes of operation different from those described in

the SAR; (2) that provisions have been made to assure that all tests

and experiments are conducted in accordance with approved written

procedures; (3) that responsibilities have been assi

and approving tests and experimental procedures; (4)gned for reviewing

that responsibilities

have been assigned to assure that controls identified above will be

implemented; (5) that a formal system has been established to assure

that all proposed tests and experiments will be reviewed to detennine

whether they are described in the FSAR; (6) that responsibilities have

,

been assigned to assure that a written safety evaluation pursuant to

10 CFR 50.59 will be developed for each test or experiment not described

!

in the SAR to assure that it does not involve unreviewed safety questions

or a change in the Technical Specification, and, (7) that responsibilities

have been assigned to assure that all tests and experiments are formally

reported to the NRC in a timely manner.

Documents Reviewed:

1.

Appendix A, Quality Assurance, Updated FSAR.

2.

Technical Specification S.5.1, Onsite Safety Committee.

3.

Technical Specification 6.5.2, Offsite Review Committee.

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4.

BVPS-1 Station Administrative Procedures (SAP).

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5.

Nuclear Division Directives.

6.

Station Engineering Procedures (SEP).

7.

Nuclear Engineering Management Procedures (NEMP).

8.

Nuclear Engineering Division (NED) Internal Instructions.

9.

A sampling of active and completed Design Change Packages.

10. A sampling of approved and completed Operational, Maintenance,

and Plant Test and Performance Procedares.

Findings:

The SAPS establish the administrative controls program that defines

the method and responsibilities for conducting plant activities and

functions, in accordance with the BVPS Technical Specification and

various ANSI standards and Reg Guides. This provides the basic

procedural requirements that apply to all work activities on all

equipment, components and systems at BVPS. Additionally, Nuclear

Division Directives provide supplemental general administrative

guidance to and control over various operations and support activities.

The SEPs provide the general guidelines to assure that maintenance

and operating procedures are prepared, approved and controlled.

Through sampling review of various maintenance and operation

procedures (Maintenance Surveillance Procedures, Calibration Pro-

cedures, Preventative Maintenance and Corrective Maintenance Pro-

cedures, Operating Surveillance Tests, ar.d Temporary Operating

Procedures), and Onsite Safety Comittee Meeting Minutes for 1983,

the inspector verified that all new procedures (and procedure changes)

were reviewed to determine their effect on nuclear safety.

Facility changes are controlled by the SEPs and reviewed to determine

whether they are safety related or constitute a design change.

Controls exist to forward all safety related modifications that

are not design changes to the OSC with written safety evaluations

for their concurrence. For those modifications that constitute

design change, a 10 CFR 50.59 Safety Evaluation is perfonried on

the design concept, which is then reviewed by the OSC and forwarded

to the Station Superintendent for final approval. The Safety

Evaluation can be performed by either the Station Engineering Group

per applicable SEP, or by the Nuclear Engineering Division per

applicable NEMP. Additionally, if the design concept is significantly

revised to the extent that it impacts on the initial Safety Evaluation,

a nc-w station modification request is issued and the review process

is initiated again.

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The OSC performs a review of all tests and experiments that

affect nuclear safety by virtue of the 10 CFR 50.59 review of

all station operation (this includes plant testing and per-

fomance) and maintenance procedures.

Facility changes, tests and experiments conducted in 1982 were

reported to the NRC by DLC letter of March 29, 1983. The material

contained in this document was reviewed by the inspector on a

sampling basis to verify program implementation. The licensee

is currently conducting an adequate review of all facility changes,

procedure changes and tests or experiments, that meets the intent

of 10 CFR 50.59. No discrepancies were identified.

10.

Radioactive Waste Transportation Activities

10 CFR 71.62(c) requires the licensee to maintain, during the life of

a package to which they pertain, quality assurance records of the

monitoring, inspection and auditing of work performance during modi-

fication, maintenance and repair of packages. The inspector reviewed

NSOC General Inspection Reports on Chem Nuclear System Casks, CN-6-75

(AL-33-90) and Cask No.14-195-H-7,12,14 for 1981 thru 1982. The

only two recorded instances of maintenance or modification activities

to those packages were:

(1) a linear indication on the eye to plate

weld which was repaired per CNS instruction on October 20, 1981

(CNS-6-75), and (2) a primary lid bolt that was drilled and tapped

per MWR 827153 on June 29, 1982. The inspector was satisfied that

the licensee is maintaining required quality assurance records of

repair and modification activities made to packages as required per

10 CFR 71.62(c). This item was discussed with a Regional health

physics specialist with regards to inspection findings detailed in

NRC Inspection Report No. 50-334/82-19.

11. Safety and Quality Classifications

The inspector reviewed licensee activities for ensuring that the as-

built quality of structures, systems and components important to safety

is maintained through various plant modifications and maintenance

activities involving procurement of replacement components. This

includes the establishment of various classifications, the criteria

by which the classification as safety related or non-safety related is

determined, and how these classifications are used for obtaining

replacement components during maintenance and obtaining new items for

station modification.

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Documents Reviewed:

Nuclear Engineering Management Procedures (NEMP)

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2.2 Classification of Structures, Systems and Components

2.3 Requests for Station Modifications

2.6 Specifications

2.7 Vendor Infonnation, Processing and Control

2.8 Handling of Design Change Packages

2.16 Safety Evaluation Procedure

3.1

Purchase Requisitions

Station Engineering Procedures (SEP)

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2.1 QA Category, QC Level and Documentation Review

2.3 Design Change Coordination

4.1 Quality Classification of Materials, Equipment and Services

- Nuclear Engineering Department Internal Instructions

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- QA Procedures

0QA Appendix B

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BVPS Maintenance Manual

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Master Equipment List

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Q*5 Program

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- ANSI Standard N45.2.13, Quality Assurance Requirements for Control

of Procurement of Items and Services for Nuclear Power Plants.

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ANSI N45.2, Quality Assurance Program Requirements for Nuclear Power

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Plants, 1971.

ANSI N18.7, Administrative Controls for Nuclear Power Plants,1972.

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Findings:

The licensee currently employs a methodology whereby each plant system

is designated either safety related or non-safety related, as it is

specified in 00A Appendix B.

For maintenance purposes, system "Q

breaks" are not yet used, and all components within a system are

treated as the system is designated. The licensee does plan to

eventually make use of Q breaks after review and acceptance of the

Q*5 program. This unapproved program, initially accepted by the

Station Superintendent in 1979, breaks down each piece of equipment

into its component parts and classifies them according to safety

function.

From 1979 - 1981, Q*5 was not updated to reflect station

design changes. The Nuclear Engineering Division is currently up-

dating the program and performing a quality verification per applicable

NEDIs prior to certification of Q*5 as a quality document.

Final

acceptance should be by the end of 1983.

Currently, a majority of the design work that involves determining the

safety and quality classifications of equipment used in design changes

and modification is being perfonned by the Station Engineering Group

in accordance with the SEPs. As the Nuclear Engineering Division

continues to staff up, those responsibilities will be transfered to

them and implemented through NEMPs that parallel the requirements and

controls already specified in the SEPs.

All maintenance work is controlled through a Maintenance Work Request

(MWR) system, whereby Operations issues the MWR and routes it to QC

for review of work scope, quality category, replacement part specification

and assignment of hold points. The MWR is then forwarded to a main-

tenance engineer for a third level of review before work is initiated,

insuring a high degree of confidence that the safety category has been

accurately determined.

The inspector reviewed the MWR maintenance history of the reactor

control and protection system, the safety injection system, the chemical

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and volume control system, and the river water system for 1982 thru

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April ,1983.

From selected MWRs involving component replacement, the

inspector tracked replacement parts thru material requisitions to the

!

original purchase order and verified that procurement quality documentation

and vendor certificates of compliance were in conformance with procurement

l

specifications established according to its safety function.

No

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deficiencies were noted.

Through discussions with the Superintendent of Licensing and Compliance,

the inspector also determined that potential generic equipment problems

identified through IE Circulars and Information Notices were reviewed

for applicability and fcrwarded to the Procurement Group for any necessary

action.

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12. Inoffice Review of Licensee Event Reports (LERs) and Onsite Followup

'

The inspector reviewed LERs submitted to the NRC:RI office to verify

that the details of the event were clearly reported, including the

accuracy of the description of cause and adequacy of corrective action.

The inspector detemined.whether further infomation was required from

i

the licensee, whether generic implications were indicated, and whether

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the event warranted onsite' follow-up. The following;LER was reviewed:

LER 83-10/99X

Diesel Driven' Fire. Pump Inoperable

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This LER satisfys the special reporting requirement of TS 3.714.1.'

The inspector reviewed corrective maintenance activities (see

Inspection Report No. 50-334/83-07) and temporary compensatory measures

(use of a portable fire pump) used during April,1983. Licer.see

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actions were acceptable.

.

13. Unresolved Items

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Unr.esolved items are matters about which more information is. required

i

to detemine whether they are acceptable, items of noncomplience or

'.

deviations. Two unresolved items were identified and are discussed

l

in cections 5 and 8 of this report. Followup on several previo'us

t

unresolved items are discussed in section 2.

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14. Exit Interview

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Meetings were held with senior facility management periodically ,\\

during the course of this inspection to discuss the inspection

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scope and findings. A sunnary of inspection findings'were also 1

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provided to the licensee at the conclusion of the report period.;

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