ML20041E791

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Annunciator Response Procedure Ann 4.14-28, Bus 8 Level Three Trip
ML20041E791
Person / Time
Site: Haddam Neck File:Connecticut Yankee Atomic Power Co icon.png
Issue date: 01/11/1982
From:
CONNECTICUT YANKEE ATOMIC POWER CO.
To:
Shared Package
ML20041E788 List:
References
ANN-4.14-28-C, NUDOCS 8203120316
Download: ML20041E791 (2)


Text

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1.0 ALARM TITLE:

Bus 8 Level Three Trip.

2.0 MODULE NUMBER:

J1.1-1 Lower.

3.0 SETPOINT

62B/1-8 agastat dropout actuated by at least two out of three selected level three units.

The level three units are set for 3940 volts.

4.0 SIGNIFICANCE

Indicates that at 3 cast two out of three level three units have failed or a low voltage exists.

I Anundervoltagetripwilloccurifasafety injection signal occurs following the low voltage actuation.

5.0 PRCCEDURE

5.1 If there is no safety injection at trip clarm will be initiated.

this time, a level three l

the operator should notify CONVEX to try and increase theOnce this alarm is rec 115KV switchyard voltage.

within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, If the voltage can't be restored 1

_ Standby within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />.the operator must bring the plant to Hot 5.2 logic is producing an output,If a safety injection signal occurs while the de

?..

the 86/1-8 lockout relay will y

operate.

This relay will operate che 27Y, 27Y1, and 27Y2 y

relays.

These relays will do the following-

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_27Y/1-8 P

Y Operate 4/EG2A (to start the diesel)

Initiate Load Shedding (via 94LS relay) 1-8 4

Trip and Lockout 4841

[,

Closc 4T5 L l Initiate Close of 52/EG2A Block Auto Start of Charging Pump P-18-1B y

Initiate Sequencing of Service Water Pu:np P-37-1B or P-37-1A 8203120316 820304 PDR ADOCK 05000213 Page 1 of 2 p

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ANN 4.14-28-C Original 27Yl/1-8 JAN 111982 Trip HPSI Pump P-15-1B Trip LPSI Pump P92B Trip Charging Pump P-18-1B 27Y2/1-8 Trip and Lockout 2T8 Trip and Lockout 8T2 When resetting these relays, it is important that the 86/1-8 b_e reset before 27Y-1-8, and that 27Y-1-9 and safety injection 4A and 4B relays be reset prior to resetting 4/EG2A.

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