IR 05000321/2002005

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IR 05000321-02-005, IR 05000366-02-005, on 09/29/2002 - 01/04/2003; Southern Nuclear Operating Company, Inc., Edwin I. Hatch, Flood Protection, Operability Evaluations, and Event Followup
ML030160008
Person / Time
Site: Hatch  Southern Nuclear icon.png
Issue date: 01/15/2003
From: Brian Bonser
NRC/RGN-II/DRP/RPB2
To: Sumner H
Southern Nuclear Operating Co
References
IR-02-005
Download: ML030160008 (31)


Text

ary 15, 2003

SUBJECT:

EDWIN I. HATCH NUCLEAR POWER PLANT - NRC INTEGRATED INSPECTION REPORT 50-321/02-05, 50-366/02-05

Dear Mr. Sumner:

On January 4, 2003, the Nuclear Regulatory Commission (NRC) completed an inspection at your Hatch Units 1 and 2. The enclosed integrated inspection report documents the inspection findings which were discussed on January 8, 2003, with Mr. P. Wells and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

This report documents two NRC-identified findings and one self-revealing finding of very low safety significance (Green) that were determined to involve violations of NRC requirements.

However, because of the very low safety significance and because the violations were entered into your corrective action program, the NRC is treating these three violations as Non-Cited Violations (NCVs) in accordance with Section VI.A.1 of the NRCs Enforcement Policy. If you contest any NCV contained in the enclosed inspection report, you should provide a response with the basis for your denial, within 30 days of the date of this inspection report, to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator, Region II; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the Edwin I. Hatch Nuclear Power Plant.

SNC 2 In accordance with 10 CFR 2.790 of the NRCs Rules of Practice, a copy of this letter and its enclosure will be available in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Brian R. Bonser, Chief Reactor Projects Branch 2 Division of Reactor Projects Docket Nos.: 50-321, 50-366 License Nos.: DPR-57, NPF-5

Enclosure:

Integrated Inspection Report 50-321/02-05, 50-366/02-05 w/Attachment

REGION II==

Docket Nos: 50-321, 50-366 License Nos: DPR-57, NPF-5 Report No: 50-321/02-05, 50-366/02-05 Licensee: Southern Nuclear Operating Company, Inc. (SNC)

Facility: E. I. Hatch Nuclear Power Plant, Units 1 & 2 Location: P.O. Box 2010 Baxley, Georgia 31515 Dates: September 29, 2002 - January 4, 2003 Inspectors: J. Munday, Senior Resident Inspector, Reactor Projects Branch 2 N. Garrett, Resident Inspector, Reactor Projects Branch 2 C. Rapp, Senior Project Engineer, Reactor Projects Branch 2 (Section 1R06)

J. Wallo, Security Inspector, Plant Support Branch (Section 4OA5.1)

P. Vandoorn, Senior Reactor Inspector, Engineering Branch 2 (Sections 1R02 and 1R17)

M. Scott, Senior Reactor Inspector, Engineering Branch 2 (Sections 1R02 and 1R17)

S. Walker, Reactor Inspector, Engineering Branch 2 (Sections 1R02 and 1R17)

W. Bearden, Reactor Inspector, Engineering Branch 2 (Section 1R12)

Approved By: Brian R. Bonser, Chief Reactor Projects Branch 2 Division of Reactor Projects Enclosure

SUMMARY OF FINDINGS

IR 05000321/2002-005, IR 05000366/2002-005; Southern Nuclear Operating Company, Inc.;

09/29/2002 - 01/04/2003; Edwin I. Hatch Nuclear Plant, Flood Protection, Operability Evaluations, and Event Followup.

The report covered a three month period of inspection by resident inspectors and announced inspections by a regional security inspector and regional reactor inspectors. Three Green non-cited violations (NCVs) were identified. The significance of most findings in indicated by their color (Green, White, Yellow, Red) using IMC 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process,

Revision 3, dated July 2000.

A. Inspector Identified Findings

Cornerstone: Mitigating Systems

Green.

The licensee had not taken prompt corrective action to replace missing Residual Heat Removal Service Water (RHRSW) piping penetration seals at the intake structure.

A non-cited violation of 10CFR50 Appendix B, Criterion XVI was identified. This finding is more than minor because the lack of penetration seals could have permitted the Plant Service Water (PSW) valve pit to flood and affected the mitigating systems cornerstone.

Because flooding of the PSW valve pit had not occurred nor were flooding conditions present, this failure to promptly correct a condition adverse to quality is of very low safety significance. (Section 1R06)

Green.

An incorrect calculation constant resulted in a non-conservative setpoint for the Unit 1 main steam line flow - high isolation setpoint.

A self-revealing non-cited violation of Technical Specification (TS) table 3.3.6.1-1 was identified. This finding is greater than minor because the actual setpoint exceeded the TS allowable value and the analytical limit, as a result of the error. However, the violation is of very low significance because the increased steam released due to the higher setpoint would not significantly impact offsite radiological dose during a main steam line break accident. (Section 4OA3.2)

Green.

The licensee did not promptly identify the cause of a failed safety relief valve (SRV). An operability evaluation written in response to the failure was not timely and did not adequately support a determination that the remaining SRVs were operable.

Consequently, this significant condition adverse to quality was not promptly corrected and adequate measures were not taken to preclude repetition.

A non-cited violation of 10CFR50 Appendix B, Criterion XVI was identified. This finding is greater than minor because the licensees operability assessment was not timely and relied primarily on unsupported engineering judgement for a determination of operable for the remaining SRVs. It also required multiple revisions when inconsistencies were identified by the inspectors. This finding was of very low significance because no loss of SRV function occurred. (Section 4OA5.1)

Licensee-Identified Violations

None

REPORT DETAILS

Summary of Plant Status

On September 30, the Unit 1A and B reactor recirculation motor generator (RRMG) sets tripped due to oil filter fouling and a subsequent decrease in oil pressure. Reactor power decreased to approximately 33% rated thermal power (RTP). Following repairs the unit was returned to 100% RTP on October 1. On October 10, the unit was shutdown to replace three main steam safety relief valves. The unit was restarted on October 14 and operated at 100%

RTP, except for planned maintenance and testing, during the remainder of this inspection period.

On October 11, Unit 2 reduced power to approximately 50% RTP due to a reduction in main condenser vacuum when two offgas valves malfunctioned. The valves were repaired and power was restored to 100% RTP later that day. The unit operated at 100% RTP, except for planned maintenance and testing, during the remainder of this inspection period.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity

1R01 Adverse Weather Protection

a. Inspection Scope

The inspectors performed a review of the cold weather and freeze protection system associated with the emergency diesel generators (EDGs), plant service water (PSW)system, condensate storage tanks, the intake structure, and fire protection system. The inspectors reviewed the licensees freeze protection procedure, DI-OPS-36-0989N, Cold Weather Checks, and used the most recently completed preventive maintenance checklist from 52PM-MEL-005-0S, Cold Weather Checks, for cold weather preparation to assess the system readiness for cold weather and the status of system deficiencies.

In addition, on November 6 and November 12 the inspectors observed the licensees response to tornado warnings in Jefferson Davis and Appling Counties to assess their implementation of procedure 34AB-Y22-002-0, Naturally Occurring Phenomena.

b. Findings

No findings of significance were identified.

1R02 Evaluations of Changes, Tests or Experiments

a. Inspection Scope

The inspectors reviewed evaluations for eight changes to confirm that the licensee had appropriately considered the conditions under which changes to the facility or procedures may be made, and tests conducted, without prior NRC approval. The inspectors reviewed additional information such as calculations, supporting analyses, the Updated Final Safety Analysis Report (UFSAR), and drawings. The eight evaluations reviewed are listed in the Attachment.

The inspectors also reviewed samples of changes such as design changes, commercial grade dedication packages, a temporary modification, and a procedure change for which the licensee had determined that evaluations were not required, to confirm that the licensees conclusions to screen out these changes were correct and consistent with 10 CFR 50.59. The 15 screened out changes reviewed are listed in the

.

The inspectors also reviewed a recent audit of the 10CFR50.59 process to confirm that problems were identified at an appropriate threshold, were entered into the corrective action process, and appropriate corrective actions had been initiated.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment

a. Inspection Scope

Partial System Walkdowns: The inspectors performed partial walkdowns of the following six systems to verify the availability of redundant or diverse systems, and components and to verify that defense-in-depth was maintained during periods when safety equipment was inoperable. The inspectors compared system configuration to the associated licensee procedures and system and component checklists to verify systems and components were correctly aligned. Additionally, the inspectors reviewed selected Condition Reports (CRs) to verify that equipment alignment issues were being identified and adequately resolved. Plant procedures and documents reviewed are listed in the

.

  • 1B, 1C, 2A, and 2C EDGs
  • 1A, 1B, 2A, and 2C EDGs
  • 2B, 2C, 2D PSW

Complete System Walkdown: The inspectors conducted a detailed review of the alignment and condition of the Unit 1 High Pressure Coolant Injection (HPCI) system.

The inspectors compared actual system configuration to the associated licensee procedures, and system and component checklists to verify systems and components were correctly aligned. In addition, the system was walked down to verify that hangers and supports were functional and in good mechanical condition and the support systems were functional. The inspectors also reviewed the system health report, CRs, and Maintenance Work Orders (MWOs) associated with the system to verify that issues were being appropriately resolved. Plant procedures and documents reviewed are listed in the Attachment.

b. Findings

No findings of significance were identified.

1R05 Fire Protection

a. Inspection Scope

The inspectors toured seven risk significant areas, identified in the licensees Independent Plant Evaluation for External Events, to assess the material condition of the fire protection and detection equipment and to verify fire protection equipment was not obstructed. The inspectors reviewed licensee procedure 40AC-ENG-008-OS, Fire Protection Program, and conducted area walkdowns to assess the licensee's control of transient combustibles. The inspectors also reviewed the Site Fire Hazards Analysis and Pre-fire Plan drawings, A-43965, sheets 23B and 25B, to verify that the necessary fire fighting equipment, such as fire extinguishers, hose stations, ladders, and communications equipment, was in place. The fire areas inspected included the following:

  • Unit 1 RPS Room and Vertical Cable Vault, Fire Area 1013
  • Unit 2 RPS Room and Vertical Cable Vault, Fire Area 2013
  • Unit 1 and 2 Vertical Cable Vault, Fire Area 0040
  • Control Building Access, Fire Area 0014K
  • Unit 1 600 Volt Switchgear Room 1D, Fire Area 1017
  • Unit 2 600 Volt Switchgear Room 1C, Fire Area 2016
  • Control Building Elevation 112', Fire Area 0001

b. Findings

No findings of significance were identified.

1R06 Flood Protection Measures

a. Inspection Scope

The inspectors reviewed the licensees internal and external flooding mitigation procedures and equipment to verify they were consistent with the licensees design requirements and risk analysis assumptions. For internal flooding, the inspectors reviewed the UFSAR and the Individual Plant Examination and walked down the areas listed below which contained risk-significant structures, systems and components below flood level to verify flood barriers were in place. Water-tight doors were observed to verify they were closed as required by licensee procedures, the locking mechanisms functioned properly, and the sealing gasket material was intact and undamaged. The inspectors reviewed selected alarm response procedures to verify alarm setpoints and setpoints for sump pump operation in areas vulnerable to flooding were consistent with the UFSAR, the setpoint index, and Technical Specifications (TS).

The inspectors discussed external flooding preparation with engineering personnel to verify preparation and compensatory measures met the licensees design requirements and risk analysis assumptions. The inspectors checked selected cable tunnels to verify the sump pumps functioned and adverse water conditions did not exist.

The inspectors reviewed a sampling of CRs to verify the licensee was identifying and correcting problems associated with flood detection and protection of SSCs. Licensee documents and drawings reviewed during the inspection are listed in the Attachment.

Areas walked down included the following:

  • Intake Structure
  • Unit 1 Vital Battery Rooms
  • Unit 2 Vital Battery Rooms
  • Unit 1 Condensate Pumps

b. Findings

Introduction:

A finding was identified in that the licensee had not taken prompt corrective action to replace missing RHRSW piping penetration seals at the intake structure.

Description:

These penetration seals are required by the Unit 2 UFSAR to prevent high level in the intake bay from flooding the PSW valve pit. The penetration seals were described as welded steel plates over both ends of the penetration. The missing penetration seals were documented in CR 2000004378 dated November 13, 2000. The licensee determined the UFSAR could not be revised because flooding of the PSW valve pit had not been analyzed in the UFSAR. The licensee initiated MWO 10004055 to install these penetration seals.

When developing the penetration seal, the licensee identified that the type of seal to be used was not described in the UFSAR. The licensee documented this issue CR 2001003959. The licensee subsequently determined the type of seal was acceptable and revised the UFSAR accordingly. The licensee issued MWO 10100454 on February 26, 2001, to seal in these penetrations. MWO 10004055 was canceled on December 11, 2001, referencing MWO 10100454.

During a walkdown of the intake structure on November 20, 2002, the inspectors observed that no RHRSW piping penetration seals had been installed and the condition of the penetrations was similar to those described in MWO 10100454.

Analysis:

This finding is more than minor because the lack of penetration seals could have permitted the PSW valve pit to flood, which would adversely affect the PSW system function, and affected the mitigating systems cornerstone. However, because flooding of the PSW valve pit had not occurred nor were flooding conditions present, this finding is of very low safety significance. The inspectors determined this finding was indicative of a potential corrective action deficiency because of the significant delay in correcting a condition adverse to quality and is noted in Section 4OA2.

Enforcement:

10CFR50 Appendix B, Criterion XVI, Corrective Action, requires, in part, that measures shall be established to assure that conditions adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and equipment, and nonconformances are promptly identified and corrected. Contrary to the above, the licensee identified this condition adverse to quality in 2000, but as late November 20, 2002, had not corrected the condition. Because this failure to promptly correct a condition adverse to quality is of very low safety significance and has been entered into the Corrective Action Program (CAP) as CR 2002011958, this violation is being treated as a non-cited violation (NCV), consistent with Section VI.A.1 of the NRC Enforcement Policy, and is identified as NCV 50-321, 366/02-05-01, Inadequate Corrective Action for Missing Penetration Seals.

1R11 Licensed Operator Requalification

a. Inspection Scope

The inspectors observed licensed operator performance during one simulator exercise, LT-SG-50447-07, Emergency Core Cooling Strainer Clogging. The inspectors reviewed licensee procedures 10AC-MGR-019-0S, Procedure Use and Adherence, and DI-OPS-59-0896N, Operations Management Expectations, to verify formality of communication, procedure usage, alarm response, control board manipulations, and supervisory oversight. The inspectors also reviewed licensee procedure 73-EP-EIP-001-0S, Emergency Classification and Initial Actions, to verify the event action level was identified and reported correctly. The inspectors attended the post exercise critiques and discussed operator performance with the instructors to verify the licensee identified issues were comparable to issues identified by the inspectors.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

Quarterly Sample: The inspectors conducted a detailed review of the Unit 1 and 2 Hydrogen and Oxygen Sampling System, and the 18 month preventive maintenance of the 1A EDG. The inspectors performed a system walkdown and interviewed the system engineers to determine the existing system configuration and deficiencies. The inspectors reviewed the system health report, MWOs, CRs, and system modifications to assess the overall system condition and maintenance related issues. Additionally, the inspectors reviewed the licensees Maintenance Rule (MR) reports and scoping documents to determine that the systems were properly scoped, in the proper maintenance rule category, and appropriate actions were being taken on the system.

Plant procedures and documents reviewed are listed in the Attachment.

Review of Maintenance Rule Periodic Assessment: The inspectors reviewed the licensees MR periodic assessment, dated June 27, 2002, which covered the period from June 1, 2000, until May 31, 2002. The assessment report was issued to satisfy paragraph (a)(3) of 10 CFR 50.65. The inspectors reviewed the report to determine if it was issued in accordance with the time requirements of the MR and included evaluation of: balancing reliability and unavailability; MR (a)(1) and (a)(2) activities; and use of industry operating experience. To verify compliance with 10 CFR 50.65, the inspectors reviewed selected MR activities covered by the assessment period from the following risk significant systems: 4160 VAC electrical breakers, HPCI, Reactor Core Isolation Cooling (RCIC), and RHRSW. The inspectors also reviewed selected maintenance rule activities associated with corrective actions for 4160 VAC electrical breakers and the RHRSW which were classified as MR (a)(1). Additionally, the inspectors reviewed CRs, quarterly system health reports, monthly site MR summary reports, and monthly system engineer MR reports issued during the period covered by the periodic assessment to determine if corrective actions for deficiencies were being appropriately addressed.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Evaluation

a. Inspection Scope

The inspectors reviewed the following licensee Plan of the Day (POD) documents to verify that plant risk was adequately assessed prior to components being removed from service or following failure of a component. In addition, when emergent work was identified, the inspectors held discussions with licensee personnel and walked down plant systems to verify actions were taken to minimize the probability of an initiating event and maintain the functional capability of mitigating systems.

  • POD for Work Week October 5 - 11, 2002
  • POD for Work Week October 12 - 18, 2002
  • POD for Work Week October 19 - 25, 2002
  • Extension of the 1A EDG Outage during Work Week November 10 - 16, 2002
  • POD for Work Week December 3 - 9, 2002

b. Findings

No findings of significance were identified.

1R14 Personnel Performance During Non-Routine Plant Evolutions

a. Inspection Scope

For the non-routine events described below, the inspectors reviewed operator logs, plant computer data, and strip charts to determine what occurred and how the operators responded, and to verify that the response was in accordance with plant procedures.

  • On September 30, the Unit 1 A and B RRMG sets tripped due to low lubricating oil pressure when the lubricating oil filter became clogged. The licensee found that a series of equipment failures allowed water from the floor drain system to enter the service air system which subsequently migrated into the RRMG lubricating oil system through the air driven oil mist eliminator. Contaminants in the water caused the oil filters to clog and the RRMG sets to trip. The inspectors observed operator performance to assess the licensees implementation of 34AB-B31-001-02, Reactor Recirculation Pump(s) Trip, or Recirc Loops Flow Mismatch.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations

a. Inspection Scope

The inspectors reviewed the following six operability evaluations to verify the licensee had adequately assessed TS operability. The inspectors also reviewed the UFSAR to verify the system or component remained available to perform its intended function. In addition, the inspectors verified compensatory measures were adequate and properly implemented.

  • Unit 1 and 2 RHRSW Pumps Minimum Flow Valve Response Due to Loss of Air, LR-REG-007-0902
  • Common Cause Failure Analysis for EDG 2C, LR-REG-010-0902
  • Unexpected IRM/APRM Overlap During October 2002 Unit 1 SRV Outage, October 2002
  • 2C EDG Operability With The Cooling Water Outlet Valve, 2P41-F339B Not Full Closed, LR-REG-004-1102

b. Findings

No findings of significance were identified.

1R16 Operator Work Arounds

a. Inspection Scope

The inspectors assessed the cumulative effects of operator workarounds on the reliability, availability, and potential for mis-operation of a system to verify that there was no increased overall plant risk. This assessment included increases of initiating event frequencies, effects on multiple mitigating systems, and the ability of operators to correctly respond to abnormal plant conditions. The inspectors used the October 16, 2002 revision of the Operations Needs, Significant Work Arounds, and Work Arounds list, during this review.

b. Findings

No findings of significance were identified.

1R17 Permanent Plant Modifications

a. Inspection Scope

Resident Observations: The inspectors reviewed the following two modifications to determine if they adversely affected the reliability or functional capability of the associated systems. The inspectors reviewed the applicable UFSAR sections and the 10CFR50.59 assessment associated with the modification to determine if the design basis of the system was affected.

  • DCR 02-033, HPCI Oil Level Switch Fuses, Unit 2
  • DCR 00-026, Delete RCIC Electronic Overspeed Trip Biennial Review: The inspectors evaluated design change request (DCR) packages and commercial grade dedication (CGD) packages for eight modifications, in the Initiating Events and Mitigating Systems cornerstone areas, to evaluate the modifications for adverse affects on system availability, reliability, and functional capability. The modifications and the associated attributes reviewed are as follows:

- Materials type/classification/pressure boundary

- Seismic considerations

- Functional requirements to support design bases for flow and pressure control

- Functional test results

- Plant procedure and critical drawing updating

- Operations training

- Materials/Replacement Components material compatibility, Code requirements, and seismic requirements

- Associated temporary modification risk assessment

- Motor cooler functional requirements

- Inspection requirements

- Functional test criteria and results

- Supporting vendor analyses

- Plant procedure and critical drawing updating

- Operations training

- Post modification testing criteria and results

- Seismic considerations

- Pump repair and installation procedure updating

- Operational pressure test criteria and results

- Seismic considerations

- Updating of drawings and affected plant procedures

- Affected flowpaths of PSW to remaining loads

- Heat Removal

- Necessary pressure boundaries reestablished

- Pre and post modification testing criteria and results

- Seismic considerations

- Operations training

- Corrective actions for post modification problems

  • TM 2-01-02, Removal of 3 Wires for Recirc Pump A LPM Nuisance Alarm (Initiating Events)

- Removal of power / current

- Supporting license basis and safety evaluation documentation

- License basis documents updated

- Emergency Diesel Generator DG trip setpoints and characteristics bounded by new setpoint

- Response time acceptance

- Updating of procedures reflect new setpoint

- Testing acceptance criteria

- Supporting vendor analyses

- Material compatibility with original design for type, classification, and dimensions

- Critical characteristics, acceptance criteria, and method of acceptance For selected modification packages, the inspectors observed the as-built configuration.

Documents reviewed included procedures, engineering calculations, modification design and implementation packages, work orders, site drawings, corrective action documents, applicable sections of the living UFSAR, supporting analyses, Technical Specifications, and design basis information.

The inspectors also reviewed the results of two recent audits covering the modifications process and reviewed 13 CRs associated with modifications to confirm that problems were identified at an appropriate threshold, were entered into the corrective action process, and appropriate corrective actions had been initiated.

b. Findings

No findings of significance were identified.

1R19 Post Maintenance Testing

a, Inspection Scope The inspectors either observed personnel performance or reviewed the test results for the following seven maintenance testing activities to verify the scope of testing demonstrated that both the work performed was correctly completed and the affected equipment was operable. The inspectors also reviewed the maintenance package to verify procedural requirements were met. The inspectors reviewed equipment status and alignment to verify the system or component was properly realigned. Plant documents reviewed are listed in the Attachment.

  • MWO 20203586, Unit 2 HPCI Oil Level Switch
  • MWO 20203578, Troubleshoot and Repair 2C EDG Generator Field Ground
  • MWO 20202166, Disassemble Check Valve 2E51F023 for Inspection

b. Findings

No findings of significance were identified.

1R20 Refueling and Outage Activities

a. Inspection Scope

The inspectors reviewed licensee records, conducted control room observations and observed selected maintenance and testing activities to verify the licensees use of risk management during the Unit 1 main steam safety relief valve replacement outage.

Monitoring of Shutdown Activities: The inspectors observed portions of the reactor shutdown, including the insertion of a manual scram, to verify implementation of licensee procedure 34GO-OPS-013-1, Normal Plant Shutdown. In addition, the reactor cooldown was monitored to verify the cooldown rates did not exceed TS requirements and that entry into shutdown cooling was in accordance with plant procedure 34SO-E11-010-1, Residual Heat Removal System.

Licensee Control of Outage Activities: The inspectors reviewed DI-OPS-57-0393N, Outage Safety Assessment, to verify the licensee was correctly maintaining required equipment in service in accordance with outage risk management. In addition, the inspectors reviewed the contingency plans and the equipment relied on for event mitigation to verify procedures and equipment were consistent with the assumptions in the Unit 1 SRV Replacement Outage Safety Assessment, October 9, 2002. In particular, the inspectors reviewed the water level control clearance, 10220214, the operating order written to control of reactor water level during the SRV maintenance, OO-01-1002S, and procedure 34AB-E11-001-1, Loss of Shutdown Cooling, to verify that means were available and mitigating methodologies were clear should shutdown cooling be lost. In addition, the inspectors verified the appropriate requirements were satisfied prior to the primary containment being opened.

Heatup and Startup Activities: The inspectors reviewed TS and licensee procedures to verify that mode change requirements were met during both shutdown and startup.

Prior to plant startup, the inspectors performed a walkdown of the drywell to verify that material conditions supported plant operations. The inspectors observed portions of unit startup, plant heatup, and power ascension to verify implementation of licensee procedure 34GO-OPS-00101, Plant Startup.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors reviewed the following six surveillance test procedures and either observed the test or reviewed test records to verify the test scope demonstrated the affected equipment was operable. The inspectors also reviewed for preconditioning of equipment, procedure adherence, and valve alignment following completion of the surveillance. The inspectors reviewed licensee procedure AG-MGR-21-0386N, Evolution and Pre-and Post-Job Brief Guidance, and attended selected briefings to verify procedure requirements were met.

  • 34SV-SUV-020-0S, Process Point, Heat Balance Accuracy Check, Thermal Limit, FFT Check, And APRM Adjustment Surveillance

b. Findings

No findings of significance were identified.

1R23 Temporary Plant Modifications

a. Inspection Scope

The inspectors reviewed the following two temporary modifications (TMM) to verify the TMM met the criteria defined in licensee procedure 40AC-ENG-018-0S, Temporary Modification Control. In addition, the inspectors reviewed the 10 CFR 50.59 evaluation using the design basis information in the UFSAR to verify the modification did not affect the safety function of the system. The inspectors walked down the modification to verify it was installed in accordance with the TMM requirements.

  • TM-02-24, Instrument Air Supply to the Unit 2 B Reactor Recirculation Motor Generator Set Oil Mist Eliminator

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification

d. Inspection Scope

The inspectors reviewed the licensees procedures and methods for compiling and reporting performance indicators (PIs). The inspectors reviewed raw PI data collected for the PIs below from October, 2001 to September, 2002 and compared graphical representations from the most recent PI report to the raw data to verify the data was correctly included in the report. The inspectors also examined a sampling of operations logs and procedures to verify the PI data was appropriately captured for inclusion into the PI report, and that the PI was calculated correctly. Additionally, the inspectors reviewed monthly operating reports and Licensee Event Reports to verify the PI data was appropriately captured for inclusion into the PI report. The inspectors compared their observations with licensee procedure, 00AC-REG-005-0S, Preparation And Reporting Of NRC PI Data, and NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Rev. 2, to verify licensee procedure requirements and industry reporting guidelines were met.

Initiating Events Cornerstone

  • Scrams With Loss of Normal Heat Removal

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems

Cross-Reference to PI&R Findings Section 1R06 describes a finding for failure to promptly correct a condition adverse to quality associated with the RHRSW piping penetration seals. Since the licensee failed to promptly correct this condition, the finding is indicative of a potential corrective action deficiency.

Section 4OA5 describes a finding for failure to promptly identify, correct, and preclude repetition of a significant condition adverse to quality associated with the failure of the J SRV . Since the licensee failed to promptly identify, correct, and preclude repetition for this condition, the finding is indicative of a potential corrective action deficiency.

4OA3 Event Followup

.1 (Closed) Licensee Event Report (LER) 50-321/2002-004: Turbine Overspeed Control

Valve of the High Pressure Coolant Injection System Fails On August 14, 2002, the HPCI system was rendered inoperable when the turbine overspeed control valve diaphragm failed. The diaphragm was replaced and the system was returned to service. The diaphragm failure was believed to be due to a manufacturing defect. The LER was reviewed by the inspectors and no findings of significance were identified. The licensee documented this failure in CR 2002008245.

.2 (Closed) LER 50-321/2002-003: Calculation Error Results in Incorrect Steam Line High

Flow Setpoints

a. Inspection Scope

The inspectors reviewed the LER and CR 2002008176, which documented this issue in the corrective action program, to verify that the corrective action was appropriate.

Additionally, General Electric Services Information Letter No. 438, which was referenced in the LER, and appropriate sections of the Updated Final Safety Analysis Report were reviewed to ensure the significance of the issue was accurately determined.

b. Findings

Introduction:

A Green self-revealing NCV of TS table 3.3.6.1-1 was identified.

Description:

Both Unit 1 and 2 setpoints for the Group 1 main steam line high flow isolation were set non-conservatively due to an incorrect setpoint calculation. The maximum Allowable Value specified in TS table 3.3.6.1-1 is 138% of rated steam flow.

The setpoint calculation error resulted in a setpoint of 144% of rated steam flow which exceeded the analytical limit of 140% of rated steam flow. The licensee determined this condition existed for approximately eight years.

Analysis:

The inspectors determined this finding was more than minor because the actual setpoint exceeded the analytical limit and affected the mitigating systems cornerstone. However, this violation was of very low significance because the increased steam that would be released due to the higher setpoint would not significantly impact offsite radiological dose during a main steam line break accident.

Enforcement:

TS Table 3.3.6.1-1, Primary Containment Isolation Instrumentation, provided a maximum allowable value of 138% of rated steam flow. Contrary to the above, the actual setpoint was found to be 144% of rated steam flow. Because this failure to comply with Technical Specification table 3.3.6.1-1 is of very low safety significance and has been entered into the licensees CAP as CR 2002008176, this finding is being treated as an NCV in accordance with Section VI.A.1 of the NRC Enforcement Policy. The finding is identified as NCV 50-321, 366/02-05-02. Calculation Error Results in Incorrect Steam Line High Flow Setpoints.

.3 (Closed) LER 50-321/2002-005: Water Level Transient Following Manual Reactor

Scram Causes Group 2 PCIS Isolation An expected Group 2 isolation occurred when the plant was manually scrammed as part of a planned shutdown on October 10, 2002. This planned shutdown is discussed in section 1R14.2. The inspectors reviewed this LER and did not identify any findings of significance. The licensee documented this actuation in CR 2002008245.

.4 (Closed) LER 50-321/2002-002: Technical Specification Required Plant Shutdown

Because of High Unidentified Reactor Coolant System Leakage On April 19, 2002, Unit 1 was shut down when unidentified leakage in the drywell exceeded the limits of Technical Specification Limiting Condition for Operation 3.4.4.

The leakage was determined to be the result of a partially stuck open SRV, 1J, releasing steam through a failed SRV tailpipe vacuum breaker. The cause of the leaking SRV is discussed in Section 4OA5.2. The SRV tailpipe vacuum breaker failed as a result of its rapid cycling due to the leakage past the J SRV. Both components were subsequently replaced and satisfactorily tested. The inspectors reviewed this LER and did not identify any findings of significance. The licensee documented the SRV tailpipe vacuum breaker failure in CR 2002008245.

4OA5 Other Activities

.1 Temporary Instruction (TI) 2515/148, Appendix A: Pre-inspection Audit for Interim

Compensatory Measures (ICMs) at Nuclear Power Plants

a. Inspection Scope

The inspectors conducted an audit of the licensees actions in response to a February 25, 2002, Order which required the licensee to implement certain interim security compensatory measures. The audit consisted of a broad-scope review of the licensees actions in response to the Order in the areas of operations, security, emergency preparedness, and information technology as well as additional elements prescribed by the TI. The inspectors selectively reviewed relevant documentation and procedures; directly observed equipment, personnel, and activities in progress; and discussed licensee actions with personnel responsible for development and implementation of the ICM actions.

The licensees activities were reviewed against the requirements of the February 25, 2002 Order; the provisions of TI 2515/148, Appendix A; the licensees response to the Order; and the provisions of the NRC-endorsed NEI Implementation Guidance, dated July 24, 2002.

b. Findings

No findings of significance were identified. A more in-depth review of the licensees implementation of the February 25, 2002 Order, utilizing Appendix B and C of TI 2515/148 will be conducted in the near future.

.2 (Closed) Unresolved Item (URI) 50-321, 366/02-04-02: Inadequate Assessment of Main

Steam Safety Relief Valve

Introduction:

A Green NCV was identified for failure to comply with 10CFR50 Appendix B, Criterion XVI related to an untimely and inadequate SRV operability assessment.

Description:

During a reactor startup on April 19, operators noted the Unit 1 J SRV tailpipe temperature was elevated and suspected of leaking. The operators manually cycled the SRV open then closed in an attempt to reseat the SRV and reduce the leakage. Instead, the SRV stuck partially open. The unit was later manually scrammed when drywell unidentified leakage increased beyond TS limits. The licensee identified that the J SRV tailpipe vacuum breaker had cycled excessively due to the SRV leakage and was allowing steam to be admitted directly into the drywell.

After repairing the tailpipe vacuum breaker and replacing the J SRV, the unit was restarted on April 22. The licensee had not determined the cause of the SRV failure prior to restart; however, the licensee justified restart on their review that no similar failures in the industry were identified. The licensee concluded that this failure was unique and replacement of the SRV was an adequate corrective action for unit restart.

To demonstrate current operability, the remaining SRVs in Unit 1 were satisfactorily cycled at normal operating pressure. However, continued operability of these SRVs was not addressed by the licensee.

On June 21, the licensee issued an operability assessment for the remaining SRVs. An inspection of the 'J SRV had identified that the retaining nut which holds the main stage disc stem to its actuating piston was not completely tight. This resulted in vibration induced wear of the valve internals, which eventually led to the SRV failure. The licensee concluded that the actual causes of the failure of the unit 'J SRV could not conclusively be determined, but age-related degradation is suspected. The licensee identified that three Unit 1 SRVs and one Unit 2 SRV were potentially degraded based on their age and the lack of previous inspections. However, based on meeting the ASME Boiler and Pressure Vessel code and TS testing requirements as well as successfully cycling the Unit 1 SRVs after restart, the licensee concluded that no operability concern with these four SRVs existed. The inspectors concluded this only justified past operability and did not address continued operability of the SRVs. Further, as documented in Integrated Inspection Report 50-321, 366/2002-004, the inspectors identified several inconsistencies with this operability assessment.

On July 19, the licensee issued a second assessment which included the results from three SRVs which were inspected during the Unit 1 refueling outage. Significant wear was observed on the disc stem threads of two of the three SRVs. Although the SRV with only minimal stem thread wear had similar in-service time as the other two valves, the licensee concluded that age-related degradation of the SRV internals, resulting after loss of torque on the piston, likely contributed to its failure to open properly or to reseat and that only valves with more severe internal wear are prone to failure, a condition very rarely reached. Although the failure was considered by the licensee to have been age related, the inspectors noted that the in-service time necessary to damage the stem and render the valve inoperable had not been determined. As a result, on August 2, the licensee issued a third operability assessment to further address this issue. While the August 2 revision provided additional inspection and technical data, the licensees conclusion for the cause of the J SRV failure had not changed appreciably. However, from this additional data the licensee determined that in addition to time in service, torque between the piston and disc stem connection must be lost, and relative motion, or vibration, must be present for this failure mode to be possible. As a result, the licensee was able to define operational in-service time limits for the remaining SRVs.

Analysis:

The inspectors determined this finding was more than minor because the licensees operability assessment was not timely, relied primarily on unsupported engineering judgement, and required multiple revisions when inconsistencies were identified by the inspectors. The licensee stated in their final assessment that the June 21 assessment was based on input from the Event Review Team (ERT), the system engineer and corporate support personnel and that the resulting operability evaluation was built primarily on engineering judgement without documenting all the technical details used to support the operability conclusions reached in the evaluation.

Regarding the July 19 assessment, the licensee stated A subsequent operability evaluation was prepared that included more of the technical information and rationale, but still relied primarily on engineering judgement as well as plant and industry operating experience regarding the reasonable expectation that the SRVs would actuate if called upon. This finding was of very low significance because no loss of SRV function occurred. The inspectors determined this finding was indicative of a potential corrective action deficiency because a significant condition adverse to quality was not promptly corrected and adequate measures were not taken to preclude repetition and is noted in Section 4OA2.

Enforcement:

The SRVs are safety-related components and serve as a boundary between the reactor coolant system and the suppression pool. The leak through the stuck open SRV constituted a breach in this boundary and was therefore considered to be a significant condition adverse to quality. 10CFR50 Appendix B, Criterion XVI requires, in part, that measures shall be established to assure that conditions adverse to quality are promptly identified and corrected. In addition, for significant conditions adverse to quality, the measures shall assure that the cause of the condition and the corrective action taken preclude repetition. Contrary to the above, the licensee did not promptly identify the cause of the failure of the J SRV. Consequently, this significant condition adverse to quality was not promptly corrected and adequate measures were not taken to preclude repetition. Because this failure to promptly correct and preclude repetition of a significant condition adverse to quality is of very low significance and has been entered into the CAP as CR 2002011958, this violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy, and is identified as NCV 50-321, 366/02-05-03, Inadequate Assessment of Main Steam Safety Relief Valve.

4OA6 Meetings, Including Exit

The inspectors presented the inspection results to Mr. P. Wells, General Manager -

Nuclear Plant and the other members of licensee management at the conclusion of the inspection on January 8, 2003. The inspectors confirmed that proprietary information was not provided or examined during the inspection.

SUPPLEMENTARY INFORMATION

KEY POINTS OF CONTACT

Licensee personnel

J. Betsill, Assistant General Manager - Plant Support
E. Burkett, Operations Support Superintendent
D. Davis, Plant Administration Manager
R. Dedrickson, Operations Manager
M. Googe, Performance Team Manager
J. Hammonds, Engineering Support Manager
G. Johnson, Safety Audit and Engineering Review Supervisor
W. Kirkley, Health Physics and Chemistry Manager
J. Lewis, Training and Emergency Preparedness Manager
D. Madison, Assistant General Manager - Plant Operations
R. Reddick, Site Emergency Preparedness Coordinator
P. Roberts, Outage and Planning Manager
J. Thompson, Nuclear Security Manager
S. Tipps, Nuclear Safety and Compliance Manager
P. Wells, General Manager - Nuclear Plant

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

50-321, 366/02-05-01 NCV Inadequate Corrective Action for Missing Penetration Seals (Section 1R06)

50-321, 366/02-05-02 NCV Calculation Error Results in Incorrect Steam Line High Flow Setpoints (section 4OA3.2)

50-321,366/02-05-03 NCV Inadequate Assessment of Main Steam Safety Relief Valve (Section 4OA5.1)

Closed

50-321, 366/02-04-01 URI Potential Inoperability of Main Steam Safety Relief Valves (Section 4OA5.1)

50-321/2002-002 LER Technical Specification Required Plant Shutdown Because of High Unidentified Reactor Coolant System Leakage (section 4OA3.4)

50-321/2002-004 LER Turbine Overspeed Control Valve of the High Pressure Coolant Injection System Fails (Section 4OA3.1)

50-321/2002-003 LER Calculation Error Results in Incorrect Steam Line High Flow Setpoints (Section 4OA3.2)

50-321/2002-005 LER Water Level Transient Following Manual Reactor Scram Causes Group 2 PCIS Isolation (Section 4OA3.3)

LIST OF DOCUMENTS REVIEWED