IR 05000277/2010003

From kanterella
Revision as of 08:23, 23 January 2018 by StriderTol (talk | contribs) (Created page by program invented by StriderTol)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search

Download: ML102170163

Text

with copies to the Regional Administrator, Region I; the Director, Office of Enforcement, U. S. NRC, Washington, DC 20555-0001; and the NRC Senior Resident Inspector at the PBAPS. In accordance with Title 10 of the Code of Federal Regulations (CFR) 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRC's document system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). Docket Nos.
50-277,50-278 License Nos.: DPR-44, DPR-56

Sincerely,Paul G. Krohn, Chief Projects Branch 4 Division of Reactor Projects

Enclosure:

Inspection Report 05000277/2010003 and 05000278/2010003 w/AUachment: Supplemental Information cc w/encl: Distribution via ListServ In accordance with Title 10 of the Code of Federal Regulations (CFR) 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRC's document system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). Distribution w/encl: (via E-mail) M. Dapas, Acting RA (Rl0RAMAIL Resource) D. Lew, Acting DRA (Rl0RAMAIL Resource) J. Clifford, DRP (Rl DRPAMAIL Resource) D. Collins, DRP (Rl DRPAMAIL Resource) D. Roberts, DRS (R1DRSMaii Resource) P. Wilson, DRS (R1DRSMaii Resource) P. Krohn, DRP A. Rosebrook, DRP E. Torres, DRP J. Bream, DRP F. Bower, DRP, SRI A. Ziedonis, DRP, RI S. Schmitt, DRP, OA L. Trocine, RI OEDO RidsNrrPMPeachBottom Resource RidsNrrDorlLpll-2 Resource ROPreportsResource@nrc.gov

Sincerely,IRA! Paul G. Krohn, Chief Projects Branch 4 Division of Reactor Projects SUNSI Review Complete: AAR (Reviewer's Initials) ML 102170163 DOC NAME:G:\DRP\BRANCH4\1nspection Reports\Peach Bottom\2010\ 2nd Qtr. Inspection\PBIR2010-003.docx After declaring this document "An Official Agency Record" it will be released to the Public. To receive a copy of this doct.Jment, indicate in the box:'C' = Copy without attachment/enclosure "En = Copy w/attachmentJenclosure"N"= No copy OFFICE mmt RIIDRP I RIIDRP I R1/DRP I NAME FBower/AAR for ARosebrookl AAR PKrohnl PGK DATE 07/30110 08/05/10 08/05/10 Docket Nos.: License Nos.: Report No.: Licensee: Facility: Location: Dates: Inspectors: Approved by: 1 U.S. NUCLEAR REGULATORY COMMISSION REGION I 50-277, 50-278 DPR-44, DPR-56 05000277/2010003 and 05000278/2010003 Exelon Generation Company, LLC Peach Bottom Atomic Power Station, Units 2 and 3 Delta, Pennsylvania April 1, 2010 through June 30, 2010 F. Bower, Senior Resident Inspector A. Ziedonis, Resident Inspector F. Arner, Senior Reactor Inspector S. Pindale, Senior Reactor Inspector L. Scholl, Senior Reactor Inspector J. Schoppy, Senior Reactor Inspector K. Young, Senior Reactor Inspector Paul G. Krohn, Chief Reactor Projects Branch 4 Division of Reactor Projects Enclosure 2

SUMMARY OF FINDINGS

......................................................................................................... 3

REPORT DETAILS

REACTOR SAFETY

............................................................................................................... 4 1 R01 Adverse Weather Protection .................................................................................. 4 1 R04 Equipment Alignment ............................................................................................. 5 1 R05 Fire Protection ........................................................................................................ 6 1 R06 Flood Protection Measures .................................................................................... 6 1 R07 Heat Sink Performance .......................................................................................... 7 1 R11 Licensed Operator Requalification Program .................... '" .................................... 8 1 R12 Maintenance Effectiveness .................................................................................... 9 1R13 Maintenance Risk Assessments and Emergent Work Control ................................ 9 1 R 15 Operability Evaluations ........................................................................................ 10 1 R18 Plant Modifications ............................................................................................... 11 1R19 Post-Maintenance Testing .................................................................................... 11 1R22 Surveillance Testing ............................................................................................. 12 1 EP6 Drill Evaluation

OTHER ACTIVITIES (OA)

.................................................................................................... 13 40A 1 Performance Indicator (PI) Verification ................................................................. 13 40A2 Identification and Resolution of Problems (PI&R) ................................................. 13 40A6 Meetings, Including Exit ........................................................................................ 16 ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

................................................................................................... A-1

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

....................................................... A-1.

LIST OF DOCUMENTS REVIEWED

....................................................................................... A-2

LIST OF ACRONYMS

...... ..................................................................................................... A-15 Enclosure
SUMMAR Y
OF [[]]
FINDIN [[]]
GS [[]]
IR 05000277/2010003,05000278/2010003; 04/01/2010 -06/30/2010; Peach Bottom Atomic Power Station (
PBAPS ), Units 2 and 3; Integrated Inspection. The report covered a three-month period of inspection by resident inspectors and announced inspections by five senior regional reactor inspectors. The
NRC 's program for overseeing the safe operation of commercial nuclear power reactors is described in

NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006. Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity None. Other Findings A violation of very low safety significance, which was identified by the licensee, has been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensee's CAP. This violation and the licensee's corrective action tracking numbers are listed in Section 40A7 of this report. Enclosure

Summary of Plant Status

4 REPORT [[]]
DETAIL [[S Unit 2 began the inspection period at 100 percent rated thermal power (RTP) where it generally remained until May 21, 2010, when a planned power reduction to 40 percent was conducted to support summer readiness maintenance and testing that included control cell friction testing and single loop operations to replace the 2 'B' reactor recirculation pump breaker. On May 25, 2010, the unit was returned to 100 percent]]
RTP where it remained until the end of the inspection period, except for brief periods to support planned testing and rod pattern adjustments. Unit 3 began the inspection period at 100 percent
RTP where it generally remained until May 14, 2010, when power was reduced to approximately 60 percent to support summer readiness maintenance and testing. On May 16, the unit was returned to 100 percent
RTP where it remained until the end of the inspection period, except for brief periods to support planned testing, rod pattern adjustments, and planned hydraulic control unit (
HCU ) maintenance. 1.
REACTO R
SAFETY "Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity 1 R01 Adverse Weather Protection ([[Inspection procedure" contains a listed "[" character as part of the property label and has therefore been classified as invalid. -3 Samples) .1 Grid Reliability (1 Sample) a. Inspection Scope The inspectors reviewed plant features and procedures for operation and continued availability of offsite and backup power systems during adverse weather (summer conditions). The inspectors reviewed communication protocols between the control room personnel and electrical system operations, as well as measures prescribed and taken to maintain the availability and reliability of these alternating current systems. Documents reviewed are listed in the Attachment. b. Findings No findings of significance were identified . . 2 External Flooding (1 External Flooding Sample) a. Inspection Scope The inspectors reviewed selected risk-important plant design features intended to protect the plant and its safety-related equipment from external flooding events. On May 24, 2010, the inspectors reviewed the Unit 3 external flood barrier breach during planned chemical maintenance treatment (clamtrol) injection into the Unit 3 service water (SW) system. The inspectors walked down the pump structure during the barrier breach condition, reviewed the barrier breach permit, reviewed the station guidance in]]
CC -

PB-201, "Hazard Barrier Control Program," and discussed the field condition with operators to verify that the station had appropriate controls in place to mitigate an Enclosure

external flood event during the barrier breach condition. The inspectors reviewed the external flood analyses in Design Bases Document (DBD) P-T-07, "External Hazards," selected sections of the Updated Final Safety Analysis Report (UFSAR), and Special Event Procedure,

SE [[-4, "Flood Procedure," to verify that the barrier breach controls were maintained in accordance with the licensing basis. Documents reviewed are listed in the Attachment. b. Findings No findings of significance were identified . . 3 Summer Seasonal Readiness Preparations (1 Seasonal Readiness Sample) a. Inspection Scope The inspectors conducted a review of]]
PBAPS 's preparations for the 2010 summer conditions to verify selected features of the plant's design were sufficient to protect mitigating systems from the effects of adverse weather. The inspectors reviewed
PBAPS 's implementation of procedure
WC [[-AA-1 07, "Seasonal Readiness," in preparation for summer season readiness. Documentation for selected risk-significant systems was reviewed to ensure that these systems would remain functional when challenged by inclement weather. During the inspection, the inspectors focused on plant specific design features and the licensee's procedures used to mitigate or respond to adverse weather conditions. The inspectors reviewed the]]
UFSAR and performance requirements for systems selected for inspection. The inspectors reviewed
CAP records to verify that the licensee was identifying adverse weather issues at an appropriate threshold and entering them into their
CAP. [[In addition, the inspectors reviewed the "Certification of 2010 Summer Readiness" memorandum dated May 14, 2010. Documents reviewed during this inspection are listed in the Attachment. The inspectors walked down the following systems and equipment: * High Pressure Service Water (]]

HPSW) Pump Room; * Emergency Service Water (ESW) Pump Room; * Emergency Booster Pump Room; and * Emergency Diesel Generator (EDG) Rooms. 1 R04 Eguipment Alignment (71111.040 -3 Samples) .1 Partial Walkdown a. Inspection Scope The inspectors performed a partial walkdown of three systems to verify the operability of redundant or diverse trains and components when safety-related equipment was inoperable. The inspectors performed walkdowns to identify any discrepancies that could impact the function of the system and potentially increase risk. The inspectors reviewed selected applicable operations procedures, walked down system components, and verified that selected breakers, valves, and support equipment were in the correct position to support system operation. Documents reviewed are listed in the Attachment. The three systems reviewed were: Enclosure

SGTS Maintenance Outage; * 2 'A' Residual Heat Removal (
RHR ) Train during 2 'B'
RHR Train Outage; and * E-4
EDG while the E-2
EDG was Out-of-Service (
OOS [[). b. Findings No findings of significance were identified. 1 R05 Fire Protection (71111.05Q -6 Samples) .1 Fire Protection -Tours a. Inspection Scope The inspectors conducted fire protection walkdowns which were focused on availability, accessibility, and the condition of firefighting equipment. The inspectors reviewed areas to assess whether]]
PBAPS had implemented the Peach Bottom Fire Protection Plan (
FPP [[) and adequately: controlled combustibles and ignition sources within the plant; maintained fire detection and suppression capability; and maintained the material condition of passive fire protection features. For the areas inspected, the inspectors also verified that]]
PBAPS had followed the Technical Requirements Manual (
TRM ) and the
FPP when compensatory measures were implemented for

OOS, degraded or inoperable fire protection equipment, systems, or features. The inspectors verified: that fire hoses and extinguishers were in their designated locations and available for immediate use; that fire detectors and sprinklers were unobstructed; that transient combustible materials were managed in accordance with plant procedures; and fire doors, dampers, and penetration seals appeared to be in satisfactory condition. Documents reviewed during the inspection are listed in the Attachment. The inspectors toured the following areas: * Unit 2 Turbine Building, Lubricating Oil Tank Room (Fire Zone 88); * Unit 2 Reactor Building, Reactor Core Isolation Coolant (RCIC) Room (Fire Zone 60); * Turbine Building Common, Radiation Chemical Area (Fire Area 78C); * Unit 2 Turbine Building, Emergency Battery Switchgear Room (Fire Area 127); * Unit 3 Turbine Building, Emergency Battery Switchgear Room (Fire Area 117); and * Radwaste Building, Unit 3 Recirculation Pump Motor Generator (MIG) Set Room (Fire Area 12C). b. Findings No findings of significance were identified. 1 R06 Flood Protection Measures (71111.06 -1 Sample) .1 Internal Flood Protection a. Inspection Scope The inspectors reviewed selected risk-important plant design features intended to protect the plant and its safety-related equipment from internal flooding events. The Enclosure

inspectors reviewed the flood analysis and

UFSAR. The inspectors walked down the Unit 3 High Pressure Coolant Injection (
HPCI ) pump room to evaluate the condition of penetration seals, watertight doors, and other internal design features to verify that they were as described in the Individual Plant Examination. The inspectors also reviewed Exelon's monitoring and control of
HPCI [[pump mechanical seal leakage in this area to ensure the leakage would not adversely impact the operability of the system. Documents reviewed are listed in the Attachment. b. Findings No findings of significance were identified. 1 R07 Heat Sink Performance (71111.07T -2 Samples) a. Inspection Scope Based on a plant specific risk assessment, previous inspections, recent operational experience, and resident inspector input, the inspectors selected the following heat sink samples: * Operation and Performance Testing of the]]
HPSW system; and * Performance of the Ultimate Heat Sink, which Included
HPSW Piping Integrity and Intake Structure Functionality. The Conowingo Pond, supplied directly from the Susquehanna River, functions as the normal heat sink for both Peach Bottom units. The
ESW and
HPSW pumps take suction from the Conowingo Pond through the
SW pump bays. The
ESW pumps are common to both units and supply cooling to the
EDG coolers. In addition,
ESW also supplies cooling to the emergency core cooling system (
ECCS ) room coolers, core spray pump motor oil coolers, and
RHR pump seal coolers. The
HPSW system for each unit provides cooling water for the
RHR heat exchangers (
HX s) under post-accident conditions. The emergency cooling tower (ECT) provides the heat sink for the related pump bays in the unlikely event that the Conowingo Dam fails or the Conowingo pond floods. The inspectors reviewed the
ESW ,
HPSW , and intake design to evaluate the adequacy of system monitoring and performance testing. The inspectors reviewed a sample of
ESW and
HPSW [[pump and valve performance tests, system health and Generic Letter (GL) 89-13 Program reports, and in-service test (1ST) vibration monitoring results for adverse trends and to verify that the systems functioned as designed. The inspectors verified that Exelon performed the pump and valve]]
IST s in accordance with American Society of Mechanical Engineers Code requirements. In addition, the inspectors reviewed Exelon's monitoring, maintenance, and testing of interface valves between safety-related
SW and non-safety related or non-seismic piping systems to ensure that adequate
SW flow is available post-accident consistent with design basis assumptions. The inspectors reviewed Exelon's buried pipe inspection and monitoring program to independently assess the condition and structural integrity of the
HPSW piping. The inspectors reviewed a sample of
HPSW pipe nondestructive examination records and intake structure inspections to ensure that Exelon appropriately identified and dispositioned any
HPSW piping or intake structure degradation. The inspectors performed an above ground walkdown of accessible areas containing buried
HP [[]]
SW and Enclosure
ESW piping to look for soil subsidence or other indications of piping leakage and/or degradation. The inspectors also directly observed the condition of
HPSW and
ESW piping in the accessible portions of the
SW pump bays, valve pits, and
EDG rooms. The inspectors reviewed Exelon's procedures and processes to control macrofouling of the
ESW and
HPSW systems. The inspectors also observed the condition of several zebra mussel monitoring locations. The inspectors reviewed Exelon's procedures for
ESW ,
HPSW , and intake structure operation; abnormal
SW [[operations; intake flooding; and for a loss of the Conowingo Pond. The inspectors verified that Exelon maintained these procedures consistent with their design and licensing basis, and that plant operators could reasonably implement the procedures as written. The inspectors independently verified that the]]
HPSW [[pump bay and intake level instrumentation, which operators rely upon for decision making, was available and functional. The inspectors also reviewed the most recent third party structural inspection of the Conowingo Dam to assess the integrity and availability of the Conowingo Pond heat sink. The inspectors walked down control room instrument panels, accessible portions of]]
HPSW piping in the turbine and reactor buildings (including the
RHR [[]]
HX s), the
ECT , the
ESW and
HPSW pumps, and the intake area (including the trash racks, outer traveling water screen room, and
SW traveling water screens) to assess the material condition and configuration control of these structures, systems and components (SSCs). The inspectors also reviewed a sample of corrective action issue reports (IRs) related to the
HPSW and
ESW isolation valves, pumps, and piping integrity to ensure that Exelon appropriately identified, characterized, and corrected problems related to these essential
SSC [[s. Documents reviewed are listed in the Attachment. b. Findings No findings of significance were identified. 1R11 Licensed Operator Regualification Program (71111.11Q -1 Sample) .1 Resident Inspector Quarterly Review a. Inspection Scope On May 3, 2010, the inspectors observed operators in]]
PBAPS [['s simulator during licensed operator requalification training to verify that operator performance was adequate and that evaluators were identifying and documenting crew performance issues. The inspectors verified that performance issues were discussed in the crew's post-scenario critiques. The inspectors discussed the training, simulator scenarios, and critiques with the operators, shift supervision, and the training instructors. The inspectors observed the following scenario: *]]
PS [[]]

EG-1109R: Evaluation Scenario. b. Findings No findings of significance were identified. Enclosure

1R12 Maintenance Effectiveness (71111.12Q -2 Samples) a. Inspection Scope The inspectors evaluated

PBAPS 's work practices and follow-up corrective actions for safety-related
SSC s and identified issues to assess the effectiveness of
PBAPS 's maintenance activities. The inspectors reviewed the performance history of
SSC s and assessed
PBAPS 's extent-of-condition (
EOC ) determinations for those issues with potential common cause or generic implications to evaluate the adequacy of the
PBAPS 's corrective actions. The inspectors assessed
PBAPS 's problem identification and resolution (PI&R) actions for these issues to evaluate whether
PBAPS had appropriately monitored, evaluated, and dispositioned the issues in accordance with Exelon procedures, including
ER -AA-310, "Implementation of the Maintenance Rule (MR)," and the requirements of 1
0 CFR 50.65, "Requirements for Monitoring the Effectiveness of Maintenance." In addition, the inspectors reviewed selected
SSC classifications, performance criteria and goals, and
PBAPS 's corrective actions that were taken or planned, to evaluate whether the actions were reasonable and appropriate. Documents reviewed are listed in the Attachment. The inspectors performed the following two samples: * 2 'C'
RHR (System 10) Exceeded
MR (a)(1) Unavailability Limit (
IR "1084973); and * Maintenance Activities Associated with Failure Mode Causal Tree (FMCT) for Tritium Leakage Mitigation Efforts (IR 1046838, Activity 6). b. Findings No findings of significance were identified. 1 R13 Maintenance Risk Assessments and Emergent Work Control ([[Inspection procedure" contains a listed "[" character as part of the property label and has therefore been classified as invalid. -6 Samples) a. Inspection Scope The inspectors evaluated]]
PBAPS 's implementation of the Maintenance Risk Program with respect to the effectiveness of risk assessments performed for maintenance activities that were conducted on
SSC s. The inspectors also verified that the licensee managed the risk in accordance with
10 CFR Part 50.65(a)(4) and procedure .
WC -AA-101, "On-line Work Control Process." The inspectors evaluated whether
PBAPS had taken the necessary steps to plan and control emergent work activities and to manage overall plant risk. The inspectors selectively reviewed

PBAPS's use of the online risk monitoring software and daily work schedules. The activities selected were based on plant maintenance schedules and systems that contributed to risk. Documents reviewed are listed in the Attachment. The inspectors completed six evaluations of maintenance activities on the following: * Control of Work and Management of Plant Risk, between April 6-7, 2010, during Partial Loss of 3 'A' Main Power Transformer Cooling (IR 1053261); * Control of Work and Management of Plant Risk, between April 26-30, during Week 1 of 5 of the 11th Annual Independent Spent Fuel Storage Installation Campaign (SF-221); Enclosure

ST [[-M-016-400-3); * Control of Work and Management of Plant Risk, between May 10-28, 2010, during Transfer of Reactor Protection System Power Supplies for Cooper Substation Tie-In to Off-Site Source 220-08 (Clearance 10000772); * Control of Work and Management of Plant Risk, between April 4-5, 2010, during on-line steam leak injection repairs to]]
CV -2-08-4018: Main Steam Supply to Recombiner System Control Valve (Operational Technical Decision Making (OTDM) associated with
IR 1045319); and * Control of Work and Management of Plant Risk during and following Identification of a Leak in the Unit 2 'C'
RHR [[]]
HX on June 16 (
RT [[-O-010-630-2). b. Findings No findings of significance were identified. 1 R15 Operability Evaluations (71111.15 -6 Samples) a. Inspection Scope The inspectors reviewed six issues to assess the technical adequacy of the operability evaluations, the use and control of compensatory measures, and compliance with the licensing and design bases. Associated adverse condition monitoring plans (ACMPs), engineering technical evaluations, and]]
OTDM documents were also reviewed. The inspectors verified these processes were performed in accordance with the applicable administrative procedures and were consistent with
NRC guidance. Specifically, the inspectors referenced procedure
OP -
AA -108-115, "Operability Determinations," and
NRC [[]]
IMC Part 9900, "Operability Determinations & Functionality Assessments for Resolutions of Degraded or Nonconforming Conditions Adverse to Quality or Safety." The inspectors also used Technical Specifications (TSs),
TRM ,
UFSAR , and associated
DBD s as references during these reviews. Documents reviewed are listed in the Attachment. The following degraded equipment issues were reviewed: * Operability Evaluation Number 10-002, Engineer Evaluation of Submerged Cable Issue (
IR 1048012); * Operability Evaluation Number 10-003, Unit
3 HPCI 30P038 Inboard and Outboard Seal Leak After Run (
IR 1048641); * Evaluate Utilization of the
2AE 018 Reactor Building Closed Cooling Water (
RBCCW )
HX with River Water Temperature Greater than 60 Degrees Fahrenheit (
AR A1552281 Evaluation 21); * Unit 2 Control Rod Drive 38-15 Double Notch (IR 1072280); *
GNF -
II Quality Update 2010-001:
GNF Bent Spacer Flow Vanes; and *

ACMP for Monitoring of 3 'B' Phase Main Power Transformer Combustible Gases (IR 1082693). b. Findings No findings of significance were identified. Enclosure

1R18 Plant Modifications (71111.18 -1 Sample) .1 Permanent Modifications a. Inspection Scope The inspectors reviewed one permanent modification to verify that modification implementation did not place the plant in an unsafe condition. The review was also conducted to verify that the design bases, licensing bases, and performance capability of risk significant

SSC s had not been degraded as a result of these modifications. The inspectors verified the modified equipment alignment through control room instrumentation observations;
UFSAR [[, drawings, procedures, and work order ryvO) reviews; staff interviews; and plant walkdowns of accessible equipment. Documents reviewed are listed in the Attachment. The following engineering change request (ECR) for a permanent modification was reviewed: *]]
ECR 07-00274, Addition of Vent Valves and Reroute of Unit 3
HPCI [[Main Pump Seal Water Line. b. Findings No findings of significance were identified. 1R19 Post-Maintenance Testing (71111.19 -5 Samples) a. Inspection Scope The inspectors observed and reviewed completed test records for selected post-maintenance testing (PMT) activities. The inspectors observed whether the tests were performed in accordance with the approved procedures or instructions and assessed the adequacy of the test methodology based on the scope of maintenance work performed. In addition, the inspectors assessed the test acceptance criteria to evaluate whether the test demonstrated that components satisfied the applicable design and licensing bases and the]]
TS requirements. The inspectors reviewed the recorded test data to verify that the acceptance criteria were satisfied. Documents reviewed are listed in the Attachment. The inspectors reviewed five
PMT s performed in conjunction with the following maintenance activities: *
RBCCW 2
AE 018
HX Replacement ryvO C0231717); * E-2
EDG Engine Inspection ryvO R1108074); * Unit 2 End-of-Cycle Recirculation Pump 'B' Trip Breaker Replacement ryvO C0299083-07); * Unit
3 HPCI Turbine Trip Level Adjustment (
IR 1060963); and * Unit 3 'B' Core Spray Pump, Valve, Flow and Cooler Functional and
1ST following Planned 'B' Loop Maintenance Outage (

ST-O-014-305-3 performed on May 19, 2010). b. Findings No findings of significance were identified. Enclosure

1R22 Surveillance Testing (71111.22-5 Samples) a. Inspection Scope (3 Routine Surveillances;

1 RCS ; and 1 1
ST [[Sample) The inspectors reviewed and observed selected portions of the following surveillance tests (STs), and compared test data with established acceptance criteria to verify the systems demonstrated the capability of performing the intended safety functions. The inspectors also verified that the systems and components maintained operational readiness, met applicable]]
TS requirements, and were capable of performing design basis functions. Documents reviewed are listed in the Attachment. The five
ST s reviewed or observed included: *
ST -O-032-301-3,
HPSW Pump, Valve and Flow Functional and
1ST [[[1 1]]
ST [[Sample]; *]]
ST [[-O-020-560-2/3, Units 2 & 3 -Reactor Coolant Leakage Test [1 Reactor Coolant System (]]
RCS [[) Leakage sample]; *]]
ST -O-010-306-3, 'B'
RHR Loop Pump, Valve, Flow, and Unit Cooler Functional and
1ST [[[1 1]]
ST [[sample]; *]]
ST -M-071-602-2, Independent Spent Fuel Storage Installation (l
SFSI ) Casks
TN -68-48 through
TN -68-64 Drying, Backfilling, and Leak Tests; and *
RT -O-023-302-2,
HPCI Turbine Overspeed Trip Reset Time Check / Adjustment and
HPCI Auxiliary Oil Pump and Manual Trip Lever Tension Test, performed on May 22,2010. The inspectors noted that
IR 1068090 was entered into the corrective action system to address a question related to the acceptance criteria contained in
RT -O-023-302-2, and verified that appropriate corrective actions were taken by
PBAPS. b. Findings No findings of significance were identified.
1EP 6 Drill Evaluation (71114.06 -1 Sample) a. Inspection Scope The inspectors evaluated the conduct of a
PBAPS emergency drill on May 10, 2010, to identify any weaknesses and deficiencies in classification and notification activities. The drill was conducted, in part, to provide drill and exercise performance (DEP) opportunities for the
DEP performance indicator (
PI [[). The inspectors observed operators respond to events in the simulator control room through the declaration and notification of an alert. The inspectors observed the operations shift manager transition emergency response command and control responsibilities to the site emergency director in the technical support center (TSC). The inspectors relocated to the]]
TSC [[to observe command and control of the emergency response organization and dose assessment as the event escalated to the declaration and notification of a site area emergency, followed by further escalation to a general emergency. The inspectors verified that the event classification and notifications were done in accordance with]]
AA -1007, "Exelon Nuclear Radiological Emergency Plan Annex for
PBAPS. " The inspectors verified that the drill evaluators correctly counted the drill's contribution in the calculation of the

DEP PI. The inspectors also verified that operations personnel in the Enclosure

simulator control room identified weaknesses or deficiencies during the critique of the drill. The following simulated events were classified during this training exercise: *

FG 1 -General Emergency, Fission Product Barrier Degradation: Fuel Cladding; *
FS 1 -Site Area Emergency, Fission Product Barrier Degradation: Primary Containment; and *
FA 1 -Alert, Fission Product Barrier Degradation: Reactor Coolant System (
RCS ). b. Findings No findings of significance were identified. 4.
OTHER [[]]
ACTIVI TIES (OA) 40A1 Performance Indicator (PI) Verification (71151 -4 Samples) Cornerstone: Barrier Integrity .1 Barrier Integrity Pis (71151 -4 Samples) a. Inspection Scope The inspectors reviewed a sample of
PBAPS 's submittals for the four Barrier Integrity Pis listed below to verify the accuracy of the data reported. The
PI definitions and the guidance contained in Nuclear Energy Institute (NEI) 99-02, "Regulatory Assessment Indicator Guideline," Revision 6, and Exelon procedure
LS -
AA -2001, "Collecting and Reporting of
NRC [[]]
PI Data," were used to verify that the reporting requirements were met. The inspectors reviewed
PI data collected from January 2009 to April 2010. The inspectors compared the graphical representations from the most recent
PI report available from the
NRC public website to the raw
PI data to verify the data was properly included in the report. The Pis reviewed were: * Unit 2 and Unit
3 RCS Specific Activity (
BI 01); and * Unit 2 and Unit
3 RCS Leakage (
BI 02). b. Findings No findings of significance were identified. 40A2 Identification and Resolution of Problems (PI&R) (71152 -1 Semi-annual Trend Sample;
1 OWA Sample) .1 Review of Items Entered into the
CAP [[a. Inspection Scope As required by Inspection Procedure (IP) 71152, "Identification and Resolution of Problems," and in order to help identify repetitive equipment failures or specific human performance issues for fOllOW-Up, the inspectors performed screening of all items entered into the licensee's]]
CAP. This was accomplished by reviewing the description of each new

AR / IR and attending daily management review committee meetings. Enclosure

b. Findings No findings of significance were identified . . 2 Semi-Annual Review to Identify Trends (1 Semi-annual Resident Inspector Sample) a. Inspection Scope The inspectors reviewed lists of

CAP items to identify trends (either
NRC or licensee identified) that might indicate the existence of a safety issue requiring more detailed inspection follow-up. The inspectors reviewed a list of approximately 6,700
IR s that
PBAPS initiated and entered into the
CAP action tracking system (Passport) from December 1, 2009 through June 1, 2010. The inspectors also reviewed a list of approximately 3,200
IR s for which corrective actions remained open. The lists were reviewed and screened to complete the required semi-annual
PI&R trend review. A sample of 54 Passport
IR [[s (listed in the Attachment) were selected from the list and reviewed in more detail to verify whether the issues were adequately identified and evaluated, and that corrective actions were either closed or planned appropriately. The inspectors evaluated the]]
IR s against the requirements of Exelon procedure,
LS -AA-125, and
10 CFR 50, Appendix B, Criterion
XVI ", "Corrective Action." b. Assessments and Observations No findings of significance were identified. The inspectors noted that during this trend review period, two significant unplanned transients occurred. One involved the trip of the 2 'A'reactor recirculation pump (IR 1026936) and the other involved a Unit 2 load reduction that was performed in response to a loss of isophase bus duct cooling ([[Issue report" contains a listed "[" character as part of the property label and has therefore been classified as invalid.). The inspectors observed that the]]
PBAPS appropriately performed root cause analyses for these two events. The inspectors also noted that
PBAPS [[performed a root cause analysis of an event involving multiple control rods that had slow scram times during the initial portions of their insertion (IR 1023827). A common cause analysiS was performed to review multiple equipment related reactivity events. The inspectors observed that the licensee appropriately used the]]
CAP and associated anal
YS is tools to evaluate reactivity management events. The inspectors observed that
PBAPS took appropriate action to perform common cause analyses of two additional areas. The first involved an adverse trend of problem identification and resolution cross-cutting aspects associated with
NRC "findings (IR 1060396). The second involved security department training and qualification failures that required remediation (IR 1061573). The inspectors also noted that maintenance personnel identified (IR 1059363) a list of historical deficiencies that supported their conclusion that poor operating reliability existed for the glycol chillers in the offgas system and contributed to adverse environmental impacts. The inspectors noted additional trends related to the following subject areas: [[Isotope" contains a listed "[" character as part of the property label and has therefore been classified as invalid. (IR 1044318,]]
IR 1024952,
IR 1032576,
IR 1030952), motor control center (
MCC ) voltages (IR 1002703,
IR 1081198,
IR 1081472,
IR 1081490,
IR 1081496), main turbine master trip solenoid valves (IR1042832,
IR 1070301,
IR 1076001), submerged cable issues (IR 1030481,
IR 1081636,
IR 1048012,
IR 1022206) and fire induced multiple spurious operations (
MSO s) related issues (IR 1053615,
IR 985851,

IR 106316, IR 1047196). The inspectors also observed a trend of aged issues that remained open Enclosure

during the inspection period that included engineering issues identified during or in preparation for

NRC inspections (
IR 707459,
IR 479833,
IR 453385,
IR 452577,
IR 451634, and
IR 762371). The inspectors had discussed these issues and trends with
PBAPS personnel. However, based on the overall review of the selected sample, the inspectors concluded that
PBAPS was: appropriately identifying and entering issues into the
CAP , adequately evaluating the identified issues, and acceptably identifying adverse trends before they became more safety significant problems . . 3 Review of Operator Work Arounds (1
OWA Sample) a. Inspection Scope As required by
IP 71152, "Identification and Resolution of Problems," the inspectors conducted a review of the
OWA program to verify that
PBAPS was identifying
OWA s problems at an appropriate threshold, have entered them in the
CAP , and proposed or implemented appropriate corrective actions. The inspectors reviewed the list of
OW As and Operator Challenges (
OC s) identified and managed in accordance with Exelon Procedure,
OP -
AA -1 02-103, "OWA Program." Specifically, the review was conducted to determine if any
OWA s for mitigating systems affected the mitigating system's safety functions or affected the operators' ability to implement abnormal and emergency operating procedures. The inspectors reviewed the following open
OWA s being tracked by
PBAPS * Unit 3 -
HPCI Pump Inboard and Outboard Seal Leakage (AR A1752639). The inspectors also reviewed the lists of open
OC s (deficiencies that are obstacles to normal plant operations), periodically walked down the panels in the main control room, and have reviewed control room deficiencies to identify and be cognizant of: (1)
OWA s that have not been evaluated by
PBAPS , and (2)

OWAs that increase the potential for personnel error, including OWAs that: * Require operations contrary to past training or require more detailed knowledge than routinely provided; * Require a change from longstanding operational practices; * Require operation of a system or component in a manner different from similar systems or components; * Create the potential for the compensatory action to be performed on equipment or under conditions for which it is not appropriate; * Impair access to required indications, increase dependence on oral communications, or require actions under adverse environmental conditions; and * Require the use of equipment and interfaces that have not been designed with consideration of the task being performed. The inspectors accompanied the Unit 2 turbine building equipment operator during dayshift rounds on June 3, 2010, and the Unit 3 reactor building nuclear equipment operator during day shift rounds on June 24, 2010, to observe any potential work around challenges. The inspectors also interviewed operators to determine if any compensatory actions they routinely take are (or should be) categorized as workarounds/challenges. Finally, the inspectors reviewed current operator turnover Enclosure

documentation to determine if there are documented compensatory actions that should be categorized as workarounds!challenges. b. Findings No findings of significance were identified. 40A6 Meetings, Including Exit .1 Commissioner Site Visit and Meeting On June 2, 2010, Commissioner

W. Magwood and members of his staff visited
PBAPS , toured the site and met with senior Exelon management. Commissioner Magwood was accompanied by Mr.
S. [[Collins, Regional Administrator, Region I and Mr. P. Krohn, Branch Chief, Region I, Division of Reactor Projects . . 2 Quarterly Resident Exit Meeting Summary On July 16,2010, the resident inspectors presented the inspection results to Mr. Thomas Dougherty and other]]
PBAPS staff, who acknowledged the findings. Mr.
P. Krohn, Chief,
USNRC [[, Region 1, Division of Reactor Projects, Branch 4, attended this quarterly inspection exit meeting. The inspectors asked the licensee whether any of the material examined during the inspection should be considered proprietary. No proprietary information was identified . . 3 Triennial Heat Sink Performance Exit Meeting Summary On May 21, 2010, the inspectors presented the inspection results to Mr. Thomas Dougherty, Site Vice President, and other members of the Exelon staff. The inspectors verified that no proprietary information was documented. 40A7 Licensee-Identified Violations The following violation of very low significance (Green) was identified by the licensee and is a violation of]]
NRC requirements which meets the criteria of Section
VI of the
NRC Enforcement Policy for being dispositioned as a
NCV * License Condition
2.C. (11).(b) requires, in part, that
PBAPS shall develop and maintain strategies for addressing large fires and explosions. On May 11, 2010, the licensee discovered that equipment used for a single mitigation strategy, described in
TSG -4.1, Attachment 15, had been removed from its designated location. The finding was assessed in accordance with
IMC 0609, Appendix L, Table 2, and determined to be of very low (Green) safety significance because the finding only impacted an individual mitigation strategy. The licensee restored the equipment and entered the issue into their
CAP as
IR 01068128.
ATIACH [[]]
MENT [[:]]
SUPPLE [[]]
MENTAL [[]]
INFORM [[]]
ATION Enclosure
SUPPLE [[]]
MENTAL [[]]
INFORM [[]]
ATION [[]]
KEY [[]]
POINTS [[]]
OF [[]]
CONTAC T Exelon Generation Company Personnel
T. [[Dougherty, Site Vice President G. Stathes, Plant Manager J. Armstrong, Regulatory Assurance Manager M. Weidman, Acting Engineering Director R. Franssen, Work Management Director J. Kovalchick, Security Manager L. Lucas, Chemistry Manager P. Navin, Operations Director R. Holmes, Radiation Protection Manager T. Wasong, Training Director J. Donell,]]
GL 89-13 Program Manager
C. Esham, System Engineer (Traveling Water Screens) W. Ford, System Engineer (
HPSW )
NRC [[Personnel P. Krohn, Branch Chief F. Bower, Senior Resident Inspector A. Ziedonis, Resident Inspector F. Arner, Senior Reactor Inspector S. Pindale, Senior Reactor Inspector L. Scholl, Senior Reactor Inspector J. Schoppy, Senior Reactor Inspector K. Young, Senior Reactor Inspector]]
LIST [[]]
OF [[]]
ITEMS [[]]
OPENED ,
CLOSED ,
AND [[]]
DISCUS SED Opened None Opened/Closed None Closed None Discussed None Attachment
LIST [[]]
OF [[]]
DOCUME [[]]
NTS [[]]
REVIEW [[]]
ED Section 1 R01: Adverse Weather Protection
SE -16, Revision 5, Grid Emergency
SE -16, Attachment A, Revision 2, Power Team Generation Dispatcher/Power System Director (PTGD/PSD) Communications to Peach Bottom
SE -16, Revision 2, Grid Emergency -Bases
OP -AA-1 08-1 07, Revision 2, Switchyard Control
OP -
AA -1 08-107-1 001 , Revision 3, Station Response to Grid Capacity Conditions
OP -
AA -1 08-107-1 002, Revision 4, Interface Agreement between Exelon Energy Delivery and Exelon Generation for Switchyard Operations
WC -
AA -107, Revision 8, Seasonal Readiness
WC -
AA -8003, Revision 1, Interface Procedure between Energy D'elivery (COMED/PECO) and Exelon Generation (Nuclear/Power) for Design Engineering and Transmission Planning Activities McDonald, John
E. ;
PECO Nuclear Station Switchyard Readiness Certification for Summer 2009, Memo to Michael Pacillio; May 15, 2009 Single Line Diagram E1, Revision 45, Station System Health Report,
DC [[Systems (Unit 2 and Unit 3), 10/1/2009 -12/31/2009 System Health Report, 4 kV (Unit 2 and Unit 3), 10/1/2009 -12/31/2009 System Health Report, Emergency Diesels, 10/1/2009 -12/31/2009 System Health Report, Station Blackout, 10/1/2009 -12/31/2009 System Health Report, Substations/Startup Sources, 10/1/2009 -12/31/2009]]
IR 891537, 2009 Summer Readiness Action Item Tracking
IR 918739, Large Transformer Summer Readiness Assessment
AIR A 1714466,
RT -O-031-91 0-3 Chemical Maintenance Treatment for
SW Systems (Spring)
CC -
PB -201, Revision 0, Hazard Barrier Control Program Drawing A-490, Revision 4, Barrier Plans: Circulating Water Pump Structure,
ECT and Diesel Generator Building P-T-07, Revision 2, External Hazards
SE -4, Revision 24, Flood Procedure
SE -4 Bases, Revision 14, Flood Procedure Bases
WO R1134802,
RT -O-031-91 0-3 Chemical Maintenance Treatment for
SW Systems (Spring) Memorandum from Thomas Dougherty to Joseph Grimes, Jr., dated May 14, 2010: Certification for 2010 Summer Readiness
RT -O-040-61 0-2, Revision 16, Outbuilding
HVAC and Equipment Inspection for Summer Operation
WC -
AA -107, Revision 8, Seasonal Readiness
IR 1048641, Unit 2
HPCI 30P038 Inboard and Outboard Seal Leak after Run
IR 1053261, 3 'A' Main Transformer Cooling Control Power Breaker Tripped
IR 1054217, Conflict between
PBAPS and Energy Delivery
HVAC Tagging
IR 1057671, Summer Readiness Contingent
WO for
DPIS -3-02-116C
IR 1059990, E4
EDG [[]]
TSA Removed from
WW 1026
IR 1065139, Maintenance Plan Closed Summer Readiness Assignments with No Action
IR 1072242, 2B

EOC/RPT Breaker Inspection Results IR 1076476, 'B' Cooling Tower Lift Pump Failed to Start Attachment

Section 1R04: Equipment Alignment

TS Surveillance Requirement Section 3.6.4.3,
SGTS Peach Bottom Protected Equipment Tracking Sheet for
2AE 018 2 'A'
RBCCW [[]]
HX and 'B'
SBGT Fan, 04/14/2010
WC -
AA -101-1004, Revision 4, Project Critique U2 'B'
RHR Loop
TSA Section 1 R05: Fire Protection
PF -60, Revision 2, Prefire Strategy Plan, Unit 2 Reactor Building,
RCIC Room -Elevation 88'-0" Fire Zone
60 PF -88, Revision 3, Prefire Strategy Plan, Unit 2 Turbine Building, Lube Oil Tank Room, Elevation 116'-0" Fire Zone 88
PF -12C, Revision 5, Prefire Strategy Plan, Unit 3 Recirculation Pump
MG Set Room, 135' Elevation, Fire Area 12C
PF -78C, Revision 5, Prefire Strategy Plan, Turbine Building Common, Radiation Chemical Area, 116' Elevation, Fire Area 78C
PF -117, Revision 6, Prefire Strategy Plan, Unit 3 Turbine Building, Emergency Battery Switchgear Rooms, 135' Elevation, Fire Area 117
PF -127, Revision 6, Prefire Strategy Plan, Unit 2 Turbine Building, Emergency Battery Switchgear Rooms, 135' Elevation, Fire Area 127 *
IR 1065158, The Legend on Drawing A-484 is Incorrect *
IR 1054609,
PF -78C and
PF -12C Need Door Identification Updated * Indicates
NRC -Identified Section 1R06: Flood Protection Measures
AO [[]]
20A. 1, Temporary Removal and Installation of Flood Barriers in the Reactor Building Drainage System, Revision 13
CR 01048641, U3
HPCI 30P038 Inboard and Outboard Seal Leak After Run
ECP 10-00151, U3
HPCI 30P038 Inboard and Outboard Seal Leak After Run
ECP 09-00160, U3
HPCI Vent Valve Installation T-103, Secondary Containment Control, Revision 16 Section 1R07: Heat Sink Performance Memo from Joseph G. Schoppy to Paul G. Krohn Thru Richard J. Conte dated June 1, 2010, regarding
PBAPS Triennial Heat Sink Performance Inspection Feeder Audits and Self-Assessments 565955,
GL 89-13 Program Functional Area Self Assessment, dated 2/28/07 703604-03,89-13 Program Check-in Assessment, dated 6/28/09 989394, Pre-
NRC Heat Sink Inspection Check-in Assessment, dated 2/24/10 Completed Surveillances
ST -O-032-301-2,
HPSW Pump, Valve and Flow FunctionaliST, performed 1/7/10
ST -O-032-301-3,
HPSW Pump, Valve and Flow FunctionaliST, performed 3/30/10
ST -O-032-635-2,
HPSW System Pressure Test Examination, performed 7/6/08, 8/11/08 & 8/13/08
ST -O-032-635-3,
HPSW System Pressure Test Examination, performed 3/4/08 & 6/7/08 Attachment
ST -0-033-300-2,
ESW , Valve, Unit Cooler, and
ECT Fans Functionali
ST , Performed 1/18/10
ST -0-033-400-2,
ESW Valve
CHK -2-33-514 1
ST , performed 9/26/08
ST -0-033-400-3,
ESW Valve
CHK -3-33-514 1
ST , performed 9/25/09 Design Basis
DBD P-S-02, Revision 12,
ESW System Design Baseline Document
DBD P-S-04, Revision 10,
HPSW System Design Baseline Document
DBD P-S-35, Revision 7, Intake Water System Design Baseline Document
DBD P-T-07, Revision 2, External Hazards Design Baseline Document Drawings 6280-M-315 Shts. 1, 2, 4, & 5, Revisions 68, 55, 53, & 57,
ESW and
HPSW Systems 6280-M-330 Sh. 1, Revision 35, Emergency Cooling System A-490 Sh. 1, Revision 4, Barrier Plan
CW. Pump Structure

IRs 304543 532363 536910 543926 574158 685077 660310 678567 708222 708248 708255 708261 708284 712457 712465 758678 758690 766675 791321 793791 793803 Miscellaneous 89-13 Program Improvement Plan, dated 6/28/09 794363 798807 805940 822594 823612 824075 824082 846746 849833 896894

899886 920405 933013

2904 1026915

26919 1026921 1058866 1071180 1071347 Equipment Operator Rounds (Unit 2 & 3 Intake Areas), dated 3/29/10 -4/4/10 G3 Wavemaker (G366) Certificate of Conformance, dated 8/8/08 & 11125/08 Inspection Report Susquehanna Electric Company Conowingo Hydroelectric Station, January

2007 PD 145404, Zebra Mussel Recommendations, dated 12/16/09 Risk-Informed Inspection Notebook for
PBAPS Unit 2 and 3, Revision 2.1a Pump Room (Room 802)
MR Walkdown Datasheet, performed 9/22/97, 3/14/01, and 11/22/06

SW (Room 806) MR Walkdown Datasheet, performed 12/16/97, 11/15/99, and Attachment

6/12/04 Unit 2 Circulating Pump Room

MR Walkdown Datasheet, performed 9/22/97, 1/25/02, and 6/28/06 Unit 2 Circulating Water 8creens
MR Walkdown Datasheet, performed 12/16/97, 11/15/99, and 6/12/04 Unit 2 8ervice Water Pump Room
MR Walkdown Datasheet, performed 9/22/97, 1/25/02, and 6/28/06 Unit 3 Circulating Pump Room
MR Walkdown Datasheet, performed 9/22/97, 1/25/02, and 6/28/06 Unit 3 Circulating Water 8creens
MR Walkdown Datasheet, performed 11/15/99 and 6/12/04 Unit 3 8ervice Water Pump Room
MR Walkdown Datasheet, performed 9/22/97, 1125/02, and 6/28/06
WC -
PB -430-1 001, 8T-0-033-400-2 Test Results Evaluation (TRE), dated 9/29/08
WO R0931744, Unit 2 & Unit 3 Intake Canal 8i1t Level Readings, performed 4/8/08 *
IR 1071837, E8W Bay Level Measurement Potentially Non-Conservative * Indicates
NRC -Identified

NDE Reports 180-2-32-4 E04 0/8, Raw Water Corrosion Ultrasonic Examination Report, dated 8/8/08 180-2-32-4 E05 0/8, Raw Water Corrosion Ultrasonic Examination Report, dated 4/15/09 180-2-32-4 E05 U/8, Raw Water Corrosion Ultrasonic Examination Report, dated 4/15/09 180-2-32-4 R03 U/8, Raw Water Corrosion Ultrasonic Examination Report, dated 8/8/08 180-2-32-4 T01 BR, Raw Water Corrosion Ultrasonic Examination Report, dated 8/8/08 180-2-32-5 E03, Raw Water Corrosion Ultrasonic Examination Report, dated 7/9/08 180-2-32-5 E03 U/8, Raw Water Corrosion Ultrasonic Examination Report, dated 1/2/09 180-2-32-5 P01, Raw Water Corrosion Ultrasonic Examination Report, dated 7/9/08 180-2-32-10 V01, Raw Water Corrosion Ultrasonic Examination Report, dated 12/8/08 180-2-32-10 V02, Raw Water Corrosion Ultrasonic Examination Report, dated 12/14/08 180-2-32-10 V04, Raw Water Corrosion Ultrasonic Examination Report, dated 12/14/08 180-2-32-10 V05, Raw Water Corrosion Ultrasonic Examination Report, dated 12/9/08 180-2-32-10 V06, Raw Water Corrosion Ultrasonic Examination Report, dated 12/14/08 180-2-32-10 V07, Raw Water Corrosion Ultrasonic Examination Report, dated 12/10/08 180-2-32-10 V08, Raw Water Corrosion Ultrasonic Examination Report, dated 12/10/08 180-3-32-6 F02 0/8, Raw Water Corrosion Ultrasonic Examination Report, dated 4/27/09 180-3-32-6 F02 U/8, Raw Water Corrosion Ultrasonic Examination Report, dated 4/27/09 180-3-32-6 F04 U/8, Raw Water Corrosion Ultrasonic Examination Report, dated 4/27/09 180-3-32-6 V03 0/8, Raw Water Corrosion Ultrasonic Examination Report, dated 4/28/09 180-3-32-6 V03 U/8, Raw Water Corrosion Ultrasonic Examination Report, dated 3/4/09 180-3-32-7 E02 U/8, Raw Water Corrosion Ultrasonic Examination Report, dated 3/4/09 180-3-32-7 F01 0/8, Raw Water Corrosion Ultrasonic Examination Report, dated 11/24/08 180-3-32-7 V03 0/8, Raw Water Corrosion Ultrasonic Examination Report, dated 4/28/09 180-3-32-10 V01, Raw Water Corrosion Ultrasonic Examination Report, dated 12/14/08 180-3-32-10 V02, Raw Water Corrosion Ultrasonic Examination Report, dated 11/18/08 180-3-32-10 V04, Raw Water Corrosion Ultrasonic Examination Report, dated 11/19/08 180-3-32-10 V05, Raw Water Corrosion Ultrasonic Examination Report, dated 11/25/08 180-3-32-10 V06, Raw Water Corrosion Ultrasonic Examination Report, dated 11/18/08 180-3-32-10 V07, Raw Water Corrosion Ultrasonic Examination Report, dated 12/16/08 180-3-32-10 V09, Raw Water Corrosion Ultrasonic Examination Report, dated 11/18/08 180-3-32-10 V10, Raw Water Corrosion Ultrasonic Examination Report, dated 12/16/08 Attachment

Report No. 0800534.401.RO, G-Scan Assessment of Various Piping Lines, dated 12/31/08 Report No. 0901287.401.R1, G-Scan Assessment of Various Safety Related Piping, December 2009 Operating Experience Generic

SW System Risk-Based Inspection Guide,
NUREG /CR-5865
EGG -2674
NRC Information Notice 2007-06: Potential Common Cause Vulnerabilities in Essential
SW Systems, dated 2/9/07
PBAPS Response to
NRC Information Notice 2007-06, dated 5/15/07 Procedures
AO 32.2-2, Revision 2,
HPSW Injection into the Reactor Vessel
AO 33.1-3, Revision 0,
ESW Bypass Valve Lineup during Shutdown of Chemical Injection System and Return to Normal
AO 33.2, Revision 6,
ESW System Manual Startup and Operations
AO 33.4-2, Revision 2,
ESW System Effluent High Radiation
AO 33.5.A, Revision 1,
RHR lCore Spray Room Cooler Flush
AO 33.6-0, Revision 1,
ESW Pump Discharge Cross-Tie Operation
COL 33.1.A-2, Revision 22,
ESW System (Unit 2 and Common)
EP -AA-1007, Revision 19, Radiological Emergency Plan Annex for
PBAPS [[]]
ER -AA-340, Revision 6,
GL 89-13 Program Implementing Procedure
ER -AA-340-1001, Revision 7,
GL 89-13 Program Implementation Instructional Guide
ER -AA-5400, Revision 2, Buried Piping and Raw Water Corrosion Program Guide
ER -
AA -5400-1 001, Revision 2, Raw Water Corrosion Program Guide
ER -
AA -5400-1002, Revision 1, Buried Piping Examination Guide
RT -0-010-660-2, Revision 10,
RHR [[]]
HX Performance Test
RT -0-031-91 0-2, Revision 17, Chemical Maintenance Treatment for Unit
2 SW Systems
RT -0-033-600-2, Revision 18, Flow Test of
ESW to
ECCS Coolers and Diesel Generator Coolers
SE -3, Revision 19, Loss of Conowingo Pond Procedure
SE -4, Revision 24, Flood Procedure
SO 32.1.A-2, Revision 14,
HPSW System Startup and Normal Operations
SO 32.2.A-2, Revision 7,
HPSW System Shutdown
SO 32.3.A-2, Revision 4,
HPSW Filling and Venting the
HPSW Side of the
RHR [[]]
HX s
SO 32.7.A-2, Revision 11, Placing Unit
2 HPSW Loops in Service Using Unit 3
HPSW Pumps
SO 32.8.A-2, Revision 6,
HPSW System Routine Inspection
SO 33.1.A, Revision 2,
ESW System Setup for Normal Standby Operation
SO 33.8.A, Revision 2,
ESW System Routine Inspection While in Standby Condition
SO 33.8.B, Revision 1,
ESW System Routine Inspection While System is in Operation System Health Reports. Maintenance History & Trending
ESW System Health Report, 4th Quarter 2009
HPSW System Health Report (Unit 2 & Unit 3), 4th Quarter 2009 Intake Silt Level Readings (In Front of Outer Screen Structure), performed 7/31/07
PBAPS [[]]
GL 89-13 Program Health Report, 4th Quarter 2009 & 1 st Quarter
2010 PBAPS Intake Canal Silt Measurements, performed 4/29/93 and 9/4190
RT -M-033-675-2, Unit 2 Pump Intake Structure Inspection and Cleaning, performed 9/28/08
RT -M-033-675-3, Unit 2 Pump Intake Structure Inspection and Cleaning, performed 9/28/09
RT -0-28B-800-2, River Temperature and Flow Monitoring, performed 4/4/10 Waterbox Debris Collected Unit 2 (Trend Data), dated 9/13/02 -1/30/10 Waterbox Debris Collected Unit 3 (Trend Data), dated 5/18/02 -3/15/09 Attachment
WO s C0223901 C0225314 C0225515 C0225614 C0229231 C0229556 C0230346 R0880510 R0916150 A-7 Section 1 R11: Licensed Operator Regualification Program
PSEG -1109R: Evaluation Scenario, Revision 2, performed 05/03/10 Section 1R12: Maintenance Effectiveness
IR 1046838, Tritium High Impact Team Action Tracking
IR 1046838, Activity 6,
FMCT [[]]
IR 1068999, Inspect / Repair / Coat Torus Drain Tank Line and Valve Pit as Required
IR 1085524, 2 'C'
RHR Floating Head Leaking
IR 1080382,
RHR [[]]
DPI -2-10-130" Indication Lowering with 2"
HPSW in Service
IR 882934, 2 'C'
RHR [[]]
HX Post-Maintenance Leakage Observed
IR 882467, Mis-measurement of 2C
RHR [[]]
HX Flange Pit Depth
IR 881590, 2
CE 024
RHR [[]]
HX Tube Side Drain Plate Cover Washed Out
IR 882367, 2 'C'
RHR Lower Outer Shell Gasket Change Learnings
WO C0233586, 2 'C'
RHR [[]]
HX Investigate/Repair/Replace
AR A 1764159,
RHR [[]]
HX A Tube to Shell Differential Pressure
WO C0220077, 2
CE 024 (2 'C'
RHR [[]]
HX ) Replace Lower (Floating) Head
AR A1546765, Testing for 2 'C'
RHR [[]]
HX Leak Section 1 R13: Maintenance Risk Assessments and Emergent Work Control
AO [[]]
50F. 3-3, Revision 5, Main Transformer High Temperature Operation
ARC -320 30C209R A-3, Revision 6, Unit 3 Generator Transformer Trouble
AR A1753947, Intermittent Main Transformer Alarm
AR A 1754304, 3 'A' Main Power Transformer Cooling Control Power Breaker Tripped
WO C0233005, Install Temporary Powerl
TCCP and Replace Breakers E-1-42-A, Sheet 3, Revision 0, Hyundai Transformer Power Control Circuit Diagram E-1-42-A, Sheet 4, Revision 0, Hyundai Transformer Power Control Circuit Diagram
IR 988387, Indicated Winding Temperature Lower Than Actual
IR 1052265, Intermittent Main Transformer Alarm
IR 1053352, 3
AX 001 Lost All Cooling for Approximately 5 Minutes
IR 1053261, 3 'A' Main Transformer Cooling Control Power Breaker Tripped Narrative Logs: April 6, 2010, Night Shift
SO [[]]
50F. 7.A-3, Revision 0, Response to 3 'A' Main Power Transformer General Trouble Alarm
IR 1044591, Procurement of
TN -68 Dry Casks
IR 1060406, Enhancement for Future
ISFSI Evaluation Risk Analysis

IR 1059078, Remove Unirradiated Fuel Channels from Peach Bottom Unit 3 Spent Fuel Pool IR 1064201, High Silica in Refuel Water Storage Tank Attachment

Narrative Logs: April 26, 2010, Night Shift; April 27, 2010, Night Shift; and April 28, 2010, Night Shift

NUREG -0612, Control of Heavy Loads at Nuclear Power Plants
SF -221, Revision 0, Spent Fuel Casks
TN -68-48 through
TN -68-64 Loading and Transport Operations
UFSAR Section 10.3, Spent Fuel Storage
AR A 1730354, Back-up N2 Supply to Automatic Depressurization System Valves
IR 1067597, Backup
ADS Nitrogen Regulators High
OOS [[]]
ST -M-016-400-3, Revision 13, Instrument Nitrogen Check Valve In-Service Test
UFSAR Section 4.4, Nuclear System Pressure Relief
UFSAR Section 10.17, Instrument Air, Service Air, and Instrument Nitrogen Systems Clearance 10000772, Tie-in of Cooper Substation to 220-08 Line
SO 60F.6.A-2, Revision 13, Transferring Reactor Protection System Power Supplies Narrative Logs: May 27,2010, Night Shift P-S-06, Revision 14, Reactor Protection System
TS and Bases Section 3.3.1.1, Reactor Protection System Instrumentation
TS and Bases Section 3.3.8.2, Reactor Protection System Electric Power Monitoring
UFSAR Section 7.2, Reactor Protection System
OTDM associated with
IR 10453119, Repair Decision for Steam Leak on
CV -2-08-4018
IR 1058291, Steam Leak on
CV -2-08-4018 has Returned
IR 1053162, U2
CV -4018 Leak Repair Exceeds Dose Estimate
TRM 3.19, Hydrogen Concentration
UFSAR Section 9.4, Gaseous Radwaste / Off-Gas System Addendum 2 to Specification 6280-M-87, Revision 1, Off-Gas Recombiners for the
PBAPS Units 2 and
3 RT -0-010-630-2, 2C
RHR [[]]
HX Leak Test, performed 06/16/10 M-010-002, Revision 12,
RHR [[]]
HX Maintenance, Section 5.8 (Bubble Test)
ACMP associated with the 2 'C'
RHR [[]]
HX Leak, dated 06/16/10
ACMP associated with the 3 'A'
RHR [[]]
HX Leak, dated 11/07/07
AO 10.9-2, Revision 4, Depressurization of the
RHR System Discharge Piping
AR A1638094,
RHR [[]]
HX 3 'A' Leak
ARC -223 20C203A, E-4, Revision 3, A
RHR [[]]
HX Tube to Shell Lo Pressure
ARC -219 20C209L, D-2, Revision 3,
HPSW Discharge Hi Radiation
CH -426, Revision 13,
HPSW System Sampling and Isotopic Analysis
IR 1080382,
DPI -2-10-130A Indication Lowering with 2 'A'
HPSW in Service
IR 1080296,
ECCS Leakage Tracking -Suggested Improvement Based on
DIER [[]]
IR 1080798,
RHR [[]]
HX Leakage for
10 CFR 100 Compliance Based on Pre-
AST [[]]
IR 1081522,
NDO Page on System Status was Inaccurate
IR 1081844, Overview Sheet Contained Incomplete
OLR Data
IR 1085385, Unexpected Alarm during 2 'C'
RHR Clearance Activities M-315, Sheet 1, Revision 68,
ESW and
HPSW [[]]
P&ID M-361, Sheet 1, Revision 81,
RHR [[]]
P&ID Narrative Control Room Logs, 06/14/10 Nightshift, 06/15/10 Dayshift, and 06/17/10 Night Shift
OTDM associated with
IR 1080382, 2 'C'
HX Leak Inspection and Repair, dated 06/16/10 Regulatory Guide 1.183, Alternate Radiological Source Terms for Evaluating DeSign Basis Accidents at Nuclear Power Reactors
SI 2D-10-91-A2Cs, Calibration Check of
RHR [[]]
HX Differential Pressure Instruments
DPT 2-10-91A and C,
DPI 2-10-130A and C, and
DPS 2-10-92A and C, performed 08/18/09
SO 32.1.A-2, Revision 14,
HPSW System Startup and Normal Operations
SO 32.3.A-2, Revision 4,
HPSW Filling and Venting the
HPSW Side of the
RHR HXs Attachment
ST -0-032-301-2,
HPSW Pump, Valve and Flow Functional and
1ST [[]]
UFSAR Section 10.7,
HPSW System
UFSAR Section 14.9.2, Current Licensing Basis Dose Evaluation Using Alternate Source Term Section 1R15: Operability Evaluations Operability Evaluation Number 10-002, Revision 0, Engineering Evaluation of Submerged Cable Issue Nuclear Event Report
NC -10-008-Y, Peach Bottom
NCV Related to Cable Condition Monitoring Program
IR 01048012, Engineering Evaluation of Submerged Cable Issue
IR 01030481,
NRC [[]]
NCV 2009005-01 -Submerged Cables Design Deficiency
IR 01054751,
NOS [[]]
ID Operations Demand for Formal Evaluations for Operability Determinations
IR 01039017,
WANO [[]]
AFI [[:]]
CM Long Term Reliability Management for Wetted Cables
OP -AA-1 08-115, Revision 9, Operability Determinations (CM-1)
ACMP for Unit 3
HPCI Seal Leakage, dated 03/27/10
IR 827889, Air Voids Identified in Various Unit 2
HPCI Lines -P2R17
IR 977203, Air Identified in Unit 3
HPCI Gland Seal Condenser Cooling Water Pipe
IR 1048641, Unit 3
HPCI 30P038 Inboard and Outboard Seal Leak After Run Operability Evaluation Number 10-003, Revision 0, Unit
3 HPCI Seal Leakage M-023-0002,
HPCI [[]]
DVMX Pump Maintenance
WO C0217821, 30P038: Replace
HPCI Pump Mechanical Seals
WO C0232672, 30P038: Perform Seal Replacement
WO C2033235, Install New Vent Valves A1611271, Unit 2 2
AE 018
RBCCW [[]]
HX Suspected Tube Leaks A1552281, Utilization of
2AE 018 with River Temperature Greater than 60 Degrees F
GNF -II Quality Update 2010-001:
GNF Bent Spacer Flow Vanes, dated 04/27/10 Part 21,
GE Hitachi Nuclear Energy: Bent Fuel Spacer Flow Wing
GE Nuclear Energy Corrective Action Request 51275, Bent Flow Tab
GE Nuclear Energy Corrective Action Request 51317, Water Rod Tab to Tab Spacing
GE Nuclear Energy Corrective Action Request 51392, Bent Flow Tab
IR 1074153, Unit 2 Control Rod Drive 38-15
HCU Directional Control Valve Requires Measurement of Adjustment Screw
AR 1761150, Unit 2 Control Rod Drive 38-15 Double Notch
AR A1762149, Unit 2 Control Rod Drive 38-15
HCU Directional Control Valve Requires Measurement of Adjustment Screw
WO M1762149, Obtain 38-15
DCV Measurement for Engineering
IR 1086595, 3 'B' Main Power Transformer Serveron O2 Gas Levels Rising
IR 1082693, 3 'B' Main Power Transformer Serveron Indicated Gas Levels Rising
AR A 1765051, 3 'B' Main Power Transformer Serveron Indicated Gas Levels Rising Section 1 R18: Plant Modifications
ECR 07-00274, Revision 0, Addition of Vent Valves and Reroute of Unit
3 HPCI Main Pump Seal Water Line 50.59 Screening Number

PB-2007-042-S, Revision 0, 50.59 Screening Associated with ECR 07-00274 Attachment

Section 1R19: Post-Maintenance Testing A1552281, Evaluate Max Re-Torque Value for

RBCCW Inlet Flange A1754274, 2 'B'
RBCCW [[]]
HX Internal Tube Leak C0231717-99, Re-Torque 2
AE 018
HX Piping/Flanges C0232897, Investigate Repair as Required C0233136, Correct Deficiencies in
OBG 013 Lower Panel
IR 1057147, Accelerated 2
BE 018
HX Degradation
IR 1060270, Visual Exam of
SW Piping Reveals Suspected Wall Thinning
IR 1062815, Piping Class
JB Gasket Selection Guidance Re: Blue-Gard Sht
IR 1064826, Lube Oil Strainer Spool Pulled Apart During Reassembly
IR 1065180, Bent Drive Pin on Tachometer Drive
IR 1066002, Corroded Connection Discovered
IR 1066427, Followup to E-2 Diesel Exciter Cabinet Cable Corroded
IR 1066888, E23 Breaker
UT Fuse Clip Female End Is Damaged
IR 1067037, Incorporate Permanent Revision
TCS to
SO 52A Procedures M-052-002, Diesel Engine Maintenance, Revision
33 RT -M-052-902-2, E2 Diesel Generator and Fuel Oil Storage Tank Inspection, Revision 6
RT -0-052-252-2, E2 Diesel Generator Inspection Post-Maintenance Functional Test, Revision
26 SO 35.6.B-2, Placing Standby
RBCCW [[]]
HX In-Service and Removing One from Service, Revision 3
ST -I-052-252-2, E-2 Diesel Generator Inspection Post-Maintenance Instrumentation and Logic Test, Revision
9 ST -I-052-262-2, E-2 Diesel Generator Inspection Post-Maintenance Handswitch Logic Test, Revision 4
ST -0-052-412-2, E2 Diesel Generator Fast Start and Full Load Test, Revision
20 ST -I-02A-406-2, Determination of 2 'B' System I End of Cycle-Recirculation Pump Trip Breaker Arc Suppression Response Time, performed
OS /23/10
ST -R-02A-400-2, End of Cycle-Recirculation Pump Trip Response Time Summation Test, Performed
OS /23/10
ACMP , Revision 1, Unit 2 'B' Recirculation Pump Trip Breaker Temperatures
OTDM Issue:
2BA 034 (3401) and (3402) Recirculation Pump Trip Breaker Heating (
IR 867732), Dated May 3,2010
IR 1072366,
PS 02 End of Shift Critique, May 21 st to 23rd D Shift
IR 1072242, 2 'B'
EOC [[]]
RPT Breaker Inspection Results
IR 1072266, New
EOC -
RPT Needs
CRL [[]]
ID and Inspection Prior to Use
RT -0-023-302-3,
HPCI Turbine Overspeed Trip Reset Time Check/Adjustment and
HPCI Auxiliary Oil Pump and Manual Trip Lever Tension Test, performed
OS /22/10 and 06/15/10
IR 1060963, Unit 3
HPCI Turbine Trip Lever Tension in Alert Range
ST -0-014-306-3, Core Spray Loop 'B' Pump, Valve, Flow, and Cooler Functional and Inservice Test, performed 05/19/2010
ST -0-014-355-3, Core Spray Loop 'B' Valve Alignment and Filled and Vented Verification, Performed 05/19/2010
IR 1069554,
MO -3-14-026B-OP Boroscopic Inspection Removed from
WW 1021
IR 1070414,
CV -3-14-034B Needs Travel Stops in Actuator
IR 1070483, Motor Connection Box Hardware Deficiencies
IR 1070880,
PCV -3-14-034B Check Valve Seated
IR 1071092, Air Voids Found During

NDE Exams of Unit 3 Core Spray Piping Attachment

Section 1 R22: Surveillance Testing M-315, Revision 52,

P&ID -
ESW and
HPSW Systems
ST -O-032-301-3, Revision 24,
HPSW Pump, Valve and Flow Functional and 1
ST , Performed 03/30/10
ST -O-020-560-2/3, Units 2 & 3 -Reactor Coolant Leakage Test
ST -O-010-306-3, Revision 30, 'B'
RHR Loop Pump, Valve, Flow, and Unit Cooler Functional and 1
ST Exelon Submittal of Registration for
IDFSI Casks #48 and #49, dated May 13, 2010 Exelon Submittal of Registration for
IDFSI Casks #50, #51 and #52, dated June 3,
2010 IR 1063429,
ISFSI Cask Vacuum Drying Duration Unexpectedly Exceeded
IR 1065100,
PS 01 End of Shift Critique for Nightshift April 30th,
2010 IR 1065390,
ISFSI Helium Leak Detector Instrument Failed
IR 1066320,
ISFSI Calibration Data Sheet Discrepancy
IR 1067335,
ISFI Vacuum Pump Float Stuck
IR 1067512, Editorial Corrections for
ISFSI [[]]
TN -68
IFSSAR and 212 Report
IR 1068443, Unusual Sheave Rotation Observed on Main Hoist Load Block
IR 1069313,
ISFSI Cask Vacuum Drying Duration Unexpectedly Exceeded
IR 1069468, Maintenance Planning Process Bypassed for Repairs of the Reactor Building Crane
IR 1069549, Historical
FME Found in the Base of the Unit 3 Fuel Prep Machine
SF -900, Revision 7,
ISFSI Abnormal Condition Response
SF -910, Revision 0, Spent Fuel Cask Leakage Location Determination
SI 2P-71-0748-XXC3, Revision 0, Channel Operational Test of
ISFSI Low Pressure Test Switches
PS -70748A and
PS -70748B, Performed 05/03/10
ST -H-071-804-2, Revision 0,
ISFSI Casks
TN -68-48 through
TN -68-52 Surface Dose Rate and Contamination, Performed 04/30/10
ST -M-071-602-2, Revision 0,
ISFSI Casks
TN -68-48 through
TN -68-64 Drying, Backfilling, and Leak Tests, Performed 04/30/10
TN -68 Generic
TS , Amendment Number 1
RT -O-023-302-2,
HPCI Turbine Overspeed Trip Reset Time Check 1 Adjustment and
HPCI Auxiliary Oil Pump and Manual Trip Lever Tension Test, performed 04/24/10, 04/30/10, and 05/22/2010 *IR 1068090,
HPCI Procedures
RT -O-023-302-2(3) should be Revised
IR 1067843,
RT -O-023-302-3 System Manager Data for past 3 years for
RT -O-023-302-2(3)
GE [[]]
SIL 392, Part 1, Revision 1, Improved
HPCI Turbine Mechanical Hydraulic Trip Design
GE [[]]
SIL 392, Part 2, Revision 1, Improved
HPCI Turbine Mechanical Hydraulic Trip Design
GE [[]]
RICSIL 37,
HPCI and
RCIS Turbine Overspeed Trip Tappet Assembly Binding * Indicates
NRC -Identified Section
1 EP 6: Drill Evaluation
EP -M-1007, Revision 19, Exelon Nuclear Radiological Emergency Plan Annex for
PBAPS [[]]
IR 1063970,
EP 01 Performance Issues Identified in 4/12
EP Drill
IR 1063984, Drill Performance S/L Notification of Site Evacuation
IR 1074430,
EP 01 05/03/10
EP Pre-Exercise
D.C. 1.5.1
FMT Briefing Attachment
PBAPS 2010 Team 5
DEP Drill Evaluation Report
PBAPS May 10, 2010 Training Drill Controller Manual Section 40A1: Performance Indicator (
PI ) Verification
LS -
AA -2001, Revision 13, Collecting and Reporting of
NRC Performance Indicators Data
LS -AA-2090, Revision 4, Monthly Data Elements for
NRC [[]]
RCS Specific Activity
LS -
AA -21 00, Revision 5, Monthly Data Elements for
NRC [[]]
RCS Leakage
ST -O-020-560-2, Revision 12, Reactor Coolant Leakage Test (sample of completed test records)
ST -O-020-560-3, Revision 14, Reactor Coolant Leakage Test (sample of completed test records)
ST -C-095-864-2, Off Gas Monitor Response and Release Rate Verification by a Grab Sample
ST -C-095-864-3, Off Gas Monitor Response and Release Rate Verification by a Grab Sample
ST -C-095-820-2, Determination of Dose Equivalent f
JC i/g 1-131 in Primary Coolant
ST -C-095-820-3, Determination of Dose Equivalent f
JC i/g 1-131 in Primary Coolant
CH -407, Sampling of Reactor Water
CH -C-601, Determination of Dose Equivalent 1-131 Section 40A2: Identification and Resolution of Problems *
IR 1 062071 ,
FSAR Change not Implemented per License Amendment
IR 1080647, 1Q10 Station Trend Review
IR 1023827, Unit 2 Control Rod (CR) Scram Times -CR Slowlinoperable
IR 1008530, Iso phase Bus Loss of Cooling Load Reduction
IR 1026936, Operations Lessons Learned frorn 2 'A' Recirc Pump Trip
IR 1020648, Common Cause Analysis for Equipment Related Reactivity Events
IR 1060396, Exelon
R. 1 Performance Indicator -Adverse Trend in
PIR -Evaluation Area
IR 707459,
EDG [[]]
GL 89-13 Testing Issues
IR 479833, No Calculation for
RCIC Oil Cooler Performance during
SBO [[]]
IR 453385, Low Margin in
HPCI [[]]
NPSH Calculation 182470-M-001
IR 452577, Lack of Allowance for Frequency Variation in
EDG Load Calc.
IR 451634,
NPSH Margin for
FSSD in Re-Rate Report
IR 705464,
EQ Temperature Affects not Considered in
MCC Control Circuit Voltage Drop
IR 1059363, Glycol Chiller Deficiencies Irnpacting Equipment Reliability
IR 1061573, Security Department Training/Qualification Failures -
CCA [[]]
IR 1044318, Corrective Actions from
IR 808183 Determined to be Ineffective
IR 1024952, Increased Trend in Tritium Levels in
MW -PB-26
IR 1032576, Elevated Tritium in Pre-Developed New Well #27 Water
IR 1030952, Unit
3 CST Heating Coil Leak, Tritium Source in Aux Steam
IR 808191, Evaluation of Unit 1 Tritium -ACE
IR 808183, Evaluation for Well #4 Tritium Increase -
ACE [[]]
IR 1086963, Torus Dewatering Tank (
TDT ) Drain valve Found Degraded
IR 1086966, Concrete Drain Valve Pit is Uncoated
IR 1087143, Coat/Seal the Unit 3 Band D
RHR Sumps
IR 1087145, Pressure Test the 3D
RHR Sump Discharge Line
IR 1087148, Perform Remote Inspection of the Recombiner Pipe Tunnel
IR 762371,
URI for Load Tap Changer Licensing Basis
IR 1002703, Insufficient Post-Loss-of-Coolant Accident
MCC Voltage for E234-T-B (6023) Attachment
IR 1081198, Low Voltage at
MCC Contactor Using
LOCA Relay Setpoints
IR 1081472, Low Voltage at
MCC Contactor Using
LOCA Relay Setpoints
IR 1081490, Low Voltage at
MCC Contactor Using
LOCA Relay Setpoints
IR 1081496, Low Voltage at
MCC Contactor Using
LOCA Relay Setpoints
IR 1081503, Low Voltage at
MCC Contactor Using
LOCA Relay Setpoints
IR 1081505, Low Voltage at
MCC Contactor Using
LOCA Relay Setpoints
IR 1081512, Low Voltage at
MCC Contactor Using
LOCA Relay Setpoints
IR 1081546, Low Voltage at
MCC Contactor Using
LOCA Relay Setpoints
IR 1081554, Low Voltage at
MCC Contactor Using
LOCA Relay Setpoints
IR 1081563, Low Voltage at
MCC Contactor Using
LOCA Relay Setpoints
IR 1081572, Low Voltage at
MCC Contactor Using
LOCA Relay Setpoints
IR 1081589, Low Voltage at
MCC Contactor Using
LOCA Relay Setpoints
IR 1081597, Low Voltage at
MCC Contactor Using
LOCA Relay Setpoints
IR 1081601, Low Voltage at
MCC Contactor Using
LOCA Relay Setpoints
IR 1081605, Low Voltage at
MCC Contactor Using
LOCA Relay Setpoints
IR 1081611, Low Voltage at
MCC Contactor Using
LOCA Relay Setpoints
IR 1030481,
NRC [[]]
NCV 2009005-01 -Submerged Cables Design Deficiency
IR 1081636,
CM [[]]
ECR Needed for Modifications for Electrical Manholes
IR 1048012, Engineering Evaluation of Submerged Cable Issue
IR 1022206, 480V Safety Related Cable Identified Submerged in Manhole
35 IR 1053615,
MSOPS 2 '0' -Failure to Trip Rx Recirc Pump on Loss of
RBC [[]]
IR 985851, Parent
IR -Coordinate Fleet Actions for
RG 1.189/NEI 00-01
IR 1063169,
MSOPS -MSO Scenarios Not Applicable to Peach Bottom
IR 1047196, Fire Protection -Multiple Spurious Operations
IR 1042832, 'B' Master Trip Solenoid Light Took 90 Seconds to Light
IR 1070301,
SV -2-01D-4896A Main Turbine
MTSV A Slow to Trip
IR 1076001, Unit
2 MTSV Harder to Reset than Normal
IR 1086613,
SV -2-01D-4896B Master Trip Solenoid Valve Not Energized
IR 1086985,
OCC Open Action Items
OP -AA-102-103, Revision 3,
OWA Program
OP -AA-102-103,
OWA and Challenges -Official List, dated 06/03/10
OP -AA-102-103,
OWA and Challenges -Closed List, dated 06/03/10
OP -AA-102-103-1001, Revision 2, Operator Burden and Operationally Significant Decisions Impact Assessment Program
OP -
PB -112-1 01-1 007, Reactor Building Equipment Operator Shift Turnover Checklist, Unit 3, 06/25/10 Night Shift
OP -
PB -112-101-1008, Turbine Building Equipment Operator Shift Turnover Checklist, Unit 2, 06/03/10, Day Shift
NER [[]]
NC -10-028 (Yellow), Importance of Understanding Circuit Breaker Control Power Indications (lR 1061366)
ST -O-098-01D-3, Revision 46, Daily Surveillance Log Mode 1, 2 or 3
ST -O-02F-560-2, Revision 13, Daily Jet Pump Operability
OWA Board Meeting Minutes, 03/30/10 Unit 2 Turbine Building Rounds List from eSoms, 06/03/10 Dayshift Unit 3 Reactor Building Rounds List from eSoms, 06/24/10 Day Shift * Indicates

NRC-identified Attachment

Section 40A7: Licensee-Identified Violations

IMC 0609, Appendix L, B.5.b Significance Determination Process
IR 1068128,
B. 5.b
PIS Inadvertently Discarded During Housekeeping
IR 1081188, B.5.b Recommended Procedural Improvements
IR 1080281, Elevation: Failure to Take Effective Corrective Actions for
B. 5.b
RT -O-100-580-2, Revision 14,
B. 5.b Tool and Material Inventory
TSG 4.1, Revision 12, Peach Bottom Station Operational Contingency Guidelines Attachment
ACMP s
ADAMS [[]]
ADS [[]]
AR [[]]
CAP [[]]
CFR [[]]
DBD [[]]
DEP [[]]
ECCS [[]]
ECR [[]]
ECT [[]]
EDG [[]]
EOC [[]]
ESW [[]]
FMCT [[]]
FPP [[]]
GL [[]]
HCU [[]]
HPCI [[]]
HPSW [[]]
HX [[]]
IMC [[]]
IP [[]]
IR [[]]
ISFSI 1
ST [[]]
MCC [[]]
MIG [[]]
MR [[]]
MSO [[]]
NCV [[]]
NDE [[]]
NEI [[]]
NRC [[]]
OC s
OOS [[]]
OTOM [[]]
OWA [[]]
PARS [[]]
PBAPS [[]]
PI [[]]
PI&R [[]]
PMT [[]]
RBCCW [[]]
RCIC [[]]
RCS [[]]
RHR [[]]
RTP A-15
LIST [[]]
OF [[]]
ACRONY [[]]
MS "Adverse Condition Monitoring Plans Agency-wide Documents Access and Management System Automatic Depressurization System Action Request Corrective Action Program Code of Federal Regulations Design Basis Document Drill and Exercise Performance Emergency Core Cooling System Engineering Change Request Emergency Cooling Tower [[system" contains a listed "[" character as part of the property label and has therefore been classified as invalid. Extent-of-Condition Emergency Service Water Failure Mode Causal Tree Fire Protection Plan Generic Letter Hydraulic Control Unit High Pressure Coolant Injection High Pressure Service Water Heat Exchanger Inspection Manual Chapter I nspection Procedure Issue Report Independent Spent Fuel Storage Installation In-Service Test Motor Control Center Motor Generator Maintenance Rule Multiple Spurious Operations Non-cited Violation Non-Destructive Examination Nuclear Energy Institute Nuclear Regulatory Commission Operator Challenges Out-of-Service Operational Technical Decision Making Operator Work Around Publicly Available Records Peach Bottom Atomic Power Station Performance Indicator Problem Identification and Resolution Post-Maintenance Testing Reactor Building Closed Cooling Water Reactor Core Isolation Coolant Reactor Coolant System Residual Heat Removal Rated Thermal Power Attachment]]
SGTS [[]]
SSC [[]]
ST s
SW [[]]
TRM [[]]
TS [[]]
TSC [[]]
UFSAR "WO A-16 Standby Gas Treatment System Structure, System, and Component Surveillance Tests Service Water Technical Requirements Manual Technical Specifications Technical Support Center [[Licensing Basis Document" contains a listed "[" character as part of the property label and has therefore been classified as invalid. Work Order Attachment]]