ML17006A012
| ML17006A012 | |
| Person / Time | |
|---|---|
| Site: | Calvert Cliffs |
| Issue date: | 12/22/2016 |
| From: | Rich Smith ITT Enidine |
| To: | Document Control Desk, Office of Nuclear Reactor Regulation |
| References | |
| 52458 | |
| Download: ML17006A012 (5) | |
Text
1212212016 U.S. Nuclear Regulatory Commission Operations Center Event Report Pagel Part 21 (PAR) Event# 52458 Rep Org: ITT ENIDINE INC. Notification Date I Time: 12/22/2016 17:35 (EST)
Supplier: ITT ENIDINE INC. Event Date I Time: 11/02/2016 (EST)
Last Modification: 12/22/2016 Region: 1 Docket#:
City: WESTMINSTER Agreement State: Yes County: License#:
State: SC NRC Notified by: RAY SMITH Notifications: JAMES NOGGLE R1DO HQ Ops Officer: DONG HWA PARK GERALD MCCOY R2DO Emergency Class: NON EMERGENCY STEVE ORTH ' R3DO 10 CFR Section: MICHAEL HAY R4DO 21.21(d)(3)(i) DEFECTS AND NONCOMPLIANCE NMSS_EVENTS_NOTIFICATI EMAIL PART 21 MATERIALS PART 21/50.55 REACTORS PART 21 - POTENTIAL TRANSDUCER COMPONENT DEFECT The following information was received via fax:
"The ITT Conoflow models GT25CA 1826 and GT25CD1826 current to pressure (l/P) transducers produce a calibrated 3.0 to 15.0 psi output pressure from a 4.0 to 20.0 mA DC (input) signal. On November 2, 2016, a discovery was made of unqualified electrical component substitutions on the internal circuit board. Supplier and internal record reviews indicate these unqualified components were used as early as May 10, 2013, as the previously qualified PCB components are no longer available. Environmental qualification of the suspect circuit boards is planned for early 2017. If any component falls to meet requirements, nuclear facilities which use this product will be advised to examine their product for unqualified printed circuit boards via notification and visual references. Qualified replacement components will be provided to all affected customers.
"Customer Name I Item Number I No.: Units Calvert Cliffs Nuclear I GT25CD1826 I 30 Control Components Inc. I GT2SCD 1826 I 3 Duke Energy Carolinas LLC I GT25CA1826 I 8 Duke Energy Carolinas LLC I GTl:SCD1826 I 4 Enertech Curtiss-Wright I GT25CA1816 I 19 Enertech Curtiss-Wright I GT25CD1826 I 4 Ergytech Inc. I GT25CA1826 I 3 Ergytech Inc. I GT25CD1826 I 3 Gefran Benelux NV I GT25CD1826 I 2 Ontario Power Generation I GT25CD1826 I 31 SPX Flow Technology I GT25CA1826 I 2 Weir Valves & Controls UK I GT25CA1826 I 78"
1212212016 U.S. Nuclear Regulatory Commission Operations Center Event Report PaJ!e I