IR 05000443/2006003
| ML062070275 | |
| Person / Time | |
|---|---|
| Site: | Seabrook |
| Issue date: | 07/25/2006 |
| From: | Paul Krohn NRC/RGN-I/DRP/PB6 |
| To: | Peschel J Florida Power & Light Energy Seabrook |
| Krohn P, RI/DRP/PB6/610-337-5120 | |
| References | |
| IR-06-003 | |
| Download: ML062070275 (37) | |
Text
July 25, 2006Mr. Gene St. PierreSite Vice President FPL Energy Seabrook, LLC Seabrook Station c/o Mr. James M. Peschel
P.O. Box 300 Seabrook, NH 03874SUBJECT:SEABROOK STATION - NRC INTEGRATED INSPECTIONREPORT 05000443/2006003Dear Mr. St. Pierre; On June 30, 2006, the Nuclear Regulatory Commission (NRC) completed an inspection at theSeabrook Nuclear Power Station. The enclosed report documents the inspection findings which were discussed on July 12, 2006, with you and members of your staff.This inspection examined activities conducted under your license as they relate to safety andcompliance with the Commission's rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.This report documents two NRC-identified findings and one self-revealing finding of very lowsafety significance (Green). These findings were determined to involve violations of NRC requirements. However, because of their very low safety significance and because they are entered into your corrective action program, the NRC is treating these findings as non-citedviolations (NCVs), in accordance with Section VI.A.1 of the NRC Enforcement Policy.If you contest any NCV in this report, you should provide a response within 30 days of the dateof this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at Seabrook.In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, itsenclosure, and your response (if any) will be available electronically for public inspection in theNRC Public Document Room or from the Publicly Available Records (PARS) com ponent of Mr. Gene St. Pierre2NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm.html (The Public Electronic Reading Room).
Sincerely,
/RA/Paul G. Krohn, ChiefProjects Branch 6 Division of Reactor ProjectsDocket No. 50-443License No: NPF-86
Enclosure:
Inspection Report No. 05000443/2006003w/ Attachment: Supplemental Information
REGION IDocket No.:05000443 License No.:NPF-86 Report No.:05000443/2006003 Licensee:Florida Power & Light Energy Seabrook, LLC (FPL)
Facility:Seabrook Station, Unit 1Location:Post Office Box 300Seabrook, New Hampshire 03874Dates:April 1, 2006 through June 30, 2006 Inspectors:Glenn Dentel, Senior Resident InspectorSteve Shaffer, Resident Inspector Scott Barber, Senior Project Engineer Barry Norris, Senior Project Engineer Nancy McNamara, Emergency Preparedness Inspector Thomas Moslak, Health Physicist Jennifer Bobiak, Reactor EngineerApproved by:Paul G. Krohn, ChiefProjects Branch 6 Division of Reactor Projects Enclosure ii
SUMMARY OF FINDINGS
IR 05000443/2006003; 4/1/2006 - 6/30/2006; Seabrook Station, Unit 1; Flood ProtectionMeasures, Personnel Performance Related to Non-Routine Plant Evolutions and Events.The report covered a 13-week period of inspection by resident inspectors, regional personnelassisting the resident staff, and an announced inspection by a regional health physics inspector. Three Green non-cited violations (NCVs) were identified. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SDP). Findings for which the SDP does notapply may be Green or be assigned a severity level after NRC management review.
TheNRC's program for overseeing the safe operation of commercial nuclear power reactors isdescribed in NUREG-1649, "Reactor Oversight Process," Revision 3, dated July 2000.A.
NRC-Identified and Self-Revealing Findings
Cornerstone: Mitigating Systems
- Green.
The inspectors identified a non-cited violation of 10 CFR 50, Appendix B,Criterion XVI, "Corrective Action" in that Seabrook did not promptly identify and correct degraded cable spreading room floor hydrostatic barriers. Seabrook identified the degraded barriers following water leakage into the essential switchgear room from an inadvertent cable spreading room deluge systemactuation on February 5, 2006. However, following the actuation, Seabrook didnot properly evaluate and implement timely compensatory measures for the degraded hydrostatic barrier to protect the essential switchgear rooms. The inspectors concluded that Seabrook had multiple opportunities including internal and external operating experience to identify the degraded barriers.The finding was more than minor because it affected the Mitigating Systemcornerstone attribute of Protection Against External Factors such as flood hazards and affected the cornerstone objective of ensuring the availability,reliability, and capability of systems that respond to initiating events. Based on adetailed evaluation of the location and condition of the degraded barriers, the finding was determined to be of very low safety significance (Green) since the flooding-related finding would not cause a plant trip or degrade two or more trains of safety systems. This finding was associated with the cross-cutting area of problem identification and resolution in that Seabrook failed to thoroughly evaluate the degraded hydrostatic barriers in the cable spreading room.
(Section 1R06.3)Green. The inspectors identified a non-cited violation of 10 CFR 50, Appendix B,Criterion XVI, "Corrective Action" in that Seabrook did not take timely corrective actions for clogged drains that support safety-related systems. In 2006,Seabrook completed an inspection of the Emergency Feedwater Pump House drains and discovered three floor drains and two of five hub drains clogged with debris. Seabrook had multiple opportunities to identify and correct the issue ivincluding: a 2000 Condition Report which identified that Seabrook had noinspection program for their drains; the initial drain inspections, some of which identified partially clogged drains; and in 2005 when the inspectors identified that the inspection program was not risk or safety-related prioritized. The inspectors concluded that Seabrook did not inspect and remediate their drains which support safety-related systems in a timely manner.The finding was more than minor because it affected the Mitigating Systemscornerstone objective to ensure the availability and reliability of systems thatrespond to initiating events to prevent undesirable consequences. The finding was determined to be of very low safety significance (Green) since the flooding-related finding would not cause a plant trip or degrade two or more trains of safety systems. This finding was associated with the cross-cutting area of problem identification and resolution in that Seabrook did not take appropriate corrective actions in a timely manner for the degraded floor drain systems in theplant. (Section 1R06.2)Green. The inspectors identified a non-cited violation of Technical Specification (TS) 3.8.2.1, "DC (Direct Current) Sources - Operating." On June 21, 2006, thebattery charger supply breaker was incorrectly opened due to a maintenance technician error. This removed the required full capacity battery charger from the 125 volt DC "B" Bus. The operators failed to properly evaluate the control room alarms on the evening of June 21, and did not recognize the degraded condition of their 125 volt DC "B" Bus for the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. A new operating crew recognized the condition and determined that the plant was in a two hour TS shutdown action statement. Seabrook had been in a condition requiring the plant to enter TS action statement 3.8.2.1 from approximately 7:00 p.m. onJune 21, 2006, until 6:20 a.m. the next morning without entering the actionstatement.The finding was more than minor because it affected the Initiating Eventscornerstone objective to limit the likelihood of events that upset plant stability dueto unreliable equipment performance. This finding was determined to be of very low safety significance (Green) since there had been an increase in the probability of an initiating event without an impact on mitigating systems, reactorcoolant system leakage, or external event initiators. This finding was associatedwith the cross-cutting area of human performance and the aspect of using human error prevention techniques since maintenance technicians opened the wrong breaker and the operators on two shifts did not identify and take the appropriate actions following the opening of the supply breaker from the battery charger to the 125 volt DC "B" Bus. (Section 1R14.1)
B.Licensee-Identified Violations
None.
Enclosure
REPORT DETAILS
Summary of Plant Status The plant began the period at full rated thermal power and operated at or near full power for theentire report period, except for approximately seven separate small power reductions (less thanthree percent, typically to outputs below 1200 Megawatts-electric) that were based on requests from the Regional Independent System Operator.2.REACTOR SAFETYCornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity1R04Equipment Alignment (71111.04).1Full System Walkdown - Service Water System (71111.04S - One Sample)
a. Inspection Scope
The inspectors conducted a detailed review of the alignment and conditions of theservice water (SW) system. The inspectors performed a walkdown to verify that the system was maintained in accordance with t he system procedures and drawings. Control room indications were verified to be appropriate and consistent with Technical Specification (TS) requirements and the Updated Final Safety Analysis Report (UFSAR).
The inspectors reviewed and evaluated the potential impact on system operation fromopen work orders, temporary modifications, condition reports, and tagged equipment.
The system health report was reviewed, verified during the walkdown, and discussedwith the system engineer.The inspectors reviewed the following documents to support the walkdowns and to verifyproper system alignment:Service Water Piping and Instrumentation Drawings 1-SW-B20792, Revision 20,1-SW-B20794, Revision 29, and 1-SW-B20795, Revision 35;Service Water System Health Reports, 4 th Quarter 2005 & 1 st Quarter 2006;Work Order 0522187 - Detectable Leakage from 1-SW-V-127;Work Order 0615037 - Interim repair to the thinned area downstream ofSW-P-41B;Operator Log Sheets;Condition Reports 04-09315, 05-07392, 05-04260, 06-03715, 06-01458,06-01065, 06-00896, 06-01458, 06-06946; andTemporary Modification 06-002, Temporary Patch on SW Outfall Line to CW,Revision 1.
b. Findings
No findings of significance were identified.
2Enclosure.2Partial System Walkdowns. (71111.04 - Five Samples)
a. Inspection Scope
The inspectors performed the following partial system walkdowns:
The 'B' containment building spray system while the 'A' containment buildingspray system was out-of-service for scheduled maintenance on April 10, 2006; The control room emergency ventilati on system following scheduled testing of the system on April 26, 2006;Safety-related portions of the main steam system in response to identifieddeficiencies with the "C" main steam isolation valve (MSIV) on May 9 and 10, 2006;The start-up feed pump which serves as a back-up to the single motor-drivenemergency feedwater pump on June 1, 2006; and*The 'B' safety injection system while the 'A' safety injection system wasout-of-service for scheduled maintenance on June 15, 2006.The inspectors conducted a walkdown of each system to verify that the critical portionsof selected systems, such as valve positions, switches, and breakers, were correctlyaligned in accordance with Seabrook's procedures and to identify any discrepancies that may have had an effect on operability. The inspectors reviewed applicable piping andinstrumentation drawings and operational lineup procedures to support the walkdowns and verify proper system alignment. Documents reviewed are listed in the attachment.
b. Findings
No findings of significance were identified.
1R05 Fire Protection (71111.05Q - Nine Samples)
a. Inspection Scope
The inspectors examined several areas of the plant to assess: 1) the control of transientcombustibles and ignition sources; 2) the operational status and material condition of the fire detection, fire suppression, and manual fire fighting equipment; 3) the material condition of the passive fire protection features (fire doors, fire dampers, fire penetration seals, etc.); and 4) the compensatory measures for out-of-service or degraded fire protection equipment. The following areas were inspected:"B" Emergency Diesel Generator Building, 21' 6" elevation;"B" Emergency Diesel Generator Building, 51' 6" elevation;"B" Emergency Diesel Generator Building, -16' 0" elevation;"B" Charging Pump Room - Primary Auxiliary Building, 7' elevation;General Area - Primary Auxiliary Building, 7' elevation;Control Building, 21' 6" elevation; "A" Emergency Switchgear Room; 3EnclosureControl Building, 21' 6" elevation; "A" & "C" 125 VDC Battery Rooms;Control Building, 21' 6" elevation; "B" Emergency Switchgear Room; andControl Building, 21' 6" elevation; "B" & "D" 125 VDC Battery Rooms.The inspectors verified that the fire areas were in accordance with applicable portions ofFire Protection Pre-Fire Strategies and Fire Hazard
Analysis.
b. Findings
No findings of significance were identified.
1R06 Flood Protection Measures (71111.06 - Three Samples).1External Flood Protection - May Heavy Rains
a. Inspection Scope
The inspectors examined Seabrook's response to heavy rains from May 12 to May 15,2006. The inspectors performed walkdowns of various plant areas to assess the impact of the heavy rains and evaluated the potential impact of closed roads in the area onemergency plan implementation. Seabrook evaluated their severe weather procedures and the ability to staff the emergency facilities. Seabrook actions were evaluatedagainst the following documents:UFSAR Section 2.4.2, "Floods;"NM 11800, "Hazardous Condition Response Plan;" andOS 1200.03, "Severe Weather Conditions."
b. Findings
No findings of significance were identified..2Untimely Corrective Actions for Degraded Floor Drains
a. Inspection Scope
The inspectors reviewed Seabrook's floor drain inspection program including inspectionresults associated with Emergency Feedwater Pump House (EFWPH) drains. The inspectors reviewed CRs 05-07320, 05-08522, 06-03866, and 06-04377 and the documents listed in the attachment. The inspectors examined Seabrook's evaluation of the impact of degraded drains, compensatory actions, and assessed the extent-of-condition review.
b. Findings
Introduction.
The inspectors identified untimely corrective actions for conductingperiodic inspections and cleaning of flood protection drains. This resulted in multiple EFWPH drains being discovered clogged with debris. This finding was determined to be of low safety significance (Green) and was characterized as a violation of 10 CFR 50, Appendix B, Criterion XVI, "Corrective Action."Description. In 2000, Seabrook initiated Condition Report (CR) 00-03137 whichidentified that the plant had not inspected or cleaned any floor drains since constructionin 1990. Seabrook developed an action plan to inspect their floor drains on a 15-year cycle. From 2000 to 2005, Seabrook identified debris and partial clogging in some ofthe inspected drains. The inspected drains did not support safety-related systems. In2005, the inspectors determined that Seabrook had not inspected the only drain systemthat is credited in their design basis, the EFWPH drains. In response to the inspectors' questions, Seabrook risk-informed the prioritization of drains to be inspected and modified their inspection procedures and methodologies. In 2006, Seabrook completed an inspection of the EFWPH drains and discovered three floor drains and two of the five hub drains clogged with debris. Additional information on inspections conducted concerning the degraded floor drains and emergency feedwater (EFW) pump operabilitywas documented in Section 1R15. Although the EFWPH drains (the designed internal flood mitigati on system) were degraded, Seabrook concluded that operability of theEFW pumps would not be impacted during an internal flooding due to the water relieving capability of a gap under an exterior door.Seabrook's failure to take timely corrective actions for clogged drains supportingsafety-related systems was a performance deficiency. The licensee had multipleopportunities to identify and correct the issue including: a 2000 condition report which identified that Seabrook had no inspection program for their drains, the initial drain inspections some of which identified partially clogged drains, and in 2005 when the inspectors identified that the inspection program was not risk prioritized.Analysis. The finding was more than minor because it affected the Mitigating Systemscornerstone objective to ensure the availability and reliability of systems that res pond toinitiating events to prevent undesirable consequences. The attributes to maintain this function include protection against external factors including floor drains that provide flood protection. The attribute was considered affected since the gap under the exterior door is not normally credited for flood protection and therefore, did not have the designcontrol to ensure availability including measurements to prevent debris buildup at thegap and ice buildup in cold weather. Using Appendix A, Phase 1 of MC 0609, the finding was determined to be of very low safety significance (Green) since the flooding related finding would not cause a plant trip or degrade two or more trains of safety systems. This conclusion was based on Seabrook's determination that the EFW pumpswould remain available during an internal flooding event.
5EnclosureThis finding was associated with the cross-cutting area of problem identification andresolution in that Seabrook did not take corrective actions in a timely manner for the degraded floor drain systems in the plant.Enforcement. 10 CFR 50, Appendix B, Criterion XVI, "Corrective Action" requires thatconditions adverse to quality are promptly identified and corrected. Contrary to the above from 2000 to 2006, Seabrook did not promptly identify and correct the degraded floor drain systems in the plant, most notably the EFWPH drains that are credited inSeabrook's design basis. Because this finding was of very low safety significance and has been entered into the Seabrook's corrective action program (CR 06-03866), this finding is being treated as an NCV consistent with Section VI.A.1 of the EnforcementPolicy (NCV 05000443/2006003-01, Untimely Corrective Actions for Degraded FloorDrains)..3Untimely Identification and Evaluation of Degraded Hydrostatic Barriers
a. Inspection Scope
In NRC Inspection Report 05000443/2006-002, an unresolved item was openedconcerning degraded cable spreading room flood seals. The inspectors reviewed various documents including the root cause (CR 06-02443), conducted extensive walkdowns of the cable spreading room and essential switchgear room, and interviewed various engineers, operators, and maintenance personnel. Documents reviewed during the inspection are listed in the Attachment. The inspectors examined Seabrook's actions to identify and repair the degraded hydrostatic barriers, evaluated the impact of the degraded barriers on the operability of the essential switchgear equipment, andassessed the extent-of-condition review. Additional information on inspections conducted concerning the degraded barriers was documented in Sections 1R06, 1R14,
1R15 , and 1R19 of NRC Inspection Report 05000443/2006-002.
b. Findings
Introduction.
Seabrook did not promptly identify and correct degraded cable spreadingroom hydrostatic barriers following water leakage into the essential switchgear room from an inadvertent cable spreading room del uge system actuation. This self-revealingfinding will be considered an NRC-identified finding due to inspector value added to theidentification and evaluation of the degraded barriers. This finding was determined to be of very low safety significance (Green) and was characterized as an NCV of 10 CFR 50, Appendix B, Criterion XVI, "Corrective Actions."Description. On February 5, 2006, the cable spreading room del uge syst eminadvertently actuated during surveillance activities. Both Seabrook and the NRCinspectors identified degraded floor penetration seals following the deluge. An extent-of-condition inspection identified that 13 of 15 floor penetration seals were degraded. Seabrook did not properly evaluate and implement timely compensatory measures for the degraded hydrostatic barrier to protect the essential switchgear rooms 6Enclosureuntil March 15, 2006, when operators isolated the fire deluge system in the cablespreading room. This action was in response to NRC questions and was approximately38 days following the deluge event and 5 days after identification of the 13 degraded seals. Subsequent inspections and evaluations identified: 1) portions of the cable spreading room were not designed to be water tight; 2) holes in seals from two removed cables; and 3) other design and qualification deficiencies. The fire protecti on syst emwas restored to operation on May 9, 2006, following re-design and repair of the design deficiencies and degraded hydrostatic barriers.The cable spreading room is located directly above both trains of essential switchgear. Therefore, an actuation of the deluge system could potentially impact both trains ofessential switchgear if the hydrostatic barriers do not perform their intended function.
UFSAR Section 9.3.3 states that in the cable spreading area "all pipe and electrical floor penetrations are sealed watertight."In the root cause evaluation, Seabrook determined the causes were: 1) during initialplant design and construction design basis requirements were not incorporated into original penetration seal specifications or cable spreading floor slab design; and 2)cables were removed from two seals and were not properly resealed. Seabrook also concluded that multiple opportunities existed to identify and correct these deficiencies; however, these opportunities were missed due to lack of engineering rigor and over-reliance on engineering judgement. Seabrook conducted extensive extent-of-condition reviews in other plant areas to address hydrostatic barriers, completed comprehensive corrective actions to seal the cable spreading rooms, and developed detailed design requirements for the cable spreading room.Seabrook's failure to identify and correct the degraded hydrostatic barriers in the cablespreading room was considered a performance deficiency. Seabrook missed multiple opportunities to identify the degraded barriers including: 1) design reviews in the 1970s and 1980s; 2) Information Notice 88-60 associated with a penetration seal event at Vogtle; 3) 1989 identification of degraded hydrostatic seals on the condensate storage tank and extent-of-condition review; 4) Information Notice 2003-08 associated with leakage through hydrostatic barriers; 5) periodic 18-month inspections of seals; and 6)
February 2006, Seabrook's inadvertent deluge of the cable spreading room.
Analysis.
The finding was more than minor because it affected the Mitigating Systemcornerstone attribute of Protection Against External Factors such as flood hazards and affected the cornerstone objective of ensuring the availability, reliability, and capability ofsystems that respond to initiating events. Using Appendix A, Phase 1 of MC 0609, thefinding was determined to be of very low safety significance (Green) since the flooding-related finding would not cause a plant trip or degrade two or more trains of safety systems. This conclusion was based on the following: 1) the amount of leakageactually experienced during the February 5, 2006, event due to an inadvertent deluge;2) a review of the degraded barriers and their location relative to essential switchgear equipment; 3) Seabrook analysis of an actuation of any fire protection deluge zone and estimated leakage rates; 4) likelihood of a fire causing an actuation; and 5) design of the essential switchgear that provides some protection against water intrusion.
7EnclosureThis finding was associated with the cross-cutting area of problem identification andresolution in that Seabrook failed to thoroughly evaluate the degraded hydrostatic barriers in the cable spreading room.Enforcement. 10 CFR 50, Appendix B, Criterion XVI, "Corrective Action" requires thatconditions adverse to quality are promptly identified and corrected. Contrary to the above from construction to 2006, Seabrook did not promptly identify that the cablespreading room floor penetration barriers were degraded from a hydrostatic barrier perspective, and did not take prompt actions to evaluate and correct the degraded condition. Because this finding was of very low safety significance and has been entered into the Seabrook's corrective action program (CRs 06-02443), this finding is being treated as an NCV consistent with Section VI.A.1 of the Enforcement Policy(NCV 05000443/2006003-02, Untimely Identification and Evaluation of DegradedHydrostatic Barriers)
.1 R07Heat Sink Performance (71111.07 - One Sample)
a. Inspection Scope
The inspectors examined the "A" and "B" emergency diesel generators jacket waterheat exchangers to determine whether the heat exchangers could fulfill their designfunctions. The inspectors reviewed past thermal performance monitoring (WO 0509597), trending data for heat exchanger temperatures and fouling factors, and ES1850.017, "SW Heat Exchanger Program," Revision 0. The inspectors interviewed
the system engineer to evaluate the process used to monitor the heat exchanger andcommitments in Generic Letter 89-13, "Service Water System Problems Affecting Safety-Related Equipment." The inspectors also reviewed condition reports to verify that issues were identified and corrected associated with the heat exchangers.
b. Findings
No findings of significance were identified.
1R11 Licensed Operator Requalification Program (71111.11)Quarterly Resident Inspector Review (71111.11Q - One Sample)
a. Inspection Scope
The inspectors observed the conduct of licensed operators during a simulator trainingsession on May 23, 2006. The inspectors reviewed the simulator's physical fidelity in order to verify similarities between the Seabrook control room and the simulator. The inspectors examined the operators' ability to perform actions associated with high-riskactivities, the Emergency Plan, previous lessons learned items, and the correct use and implementation of procedures. The inspectors observed the training evaluator's critique 8Enclosureof the operators' performance and verified that deficiencies were adequately identifiedand discussed.
b. Findings
No findings of significance were identified.
1R12 Maintenance Effectiveness (71111.12)
a. Inspection Scope
(71111.12Q - Two Samples)The inspectors evaluated maintenance rule implementation for the main steam andservice water systems. The inspectors reviewed a January 5, 2006, main steam system health report and notedthat two failures of the main steam dump controllers were characterized as maintenance rule functional failures. The inspectors interviewed engineers, reviewed specific maintenance rule criteria, and examined condition reports and associated corrective actions.The inspectors reviewed the 4 th Quarter 2005 and 1 st Quarter 2006 service water systemhealth reports. The inspectors interviewed the system engineer and reviewed specificmaintenance rule criteria, condition reports and their corrective actions. The inspectors also reviewed two work packages for the service water system and observed the fieldwork associated with the work packages.The inspectors reviewed the effectiveness of maintenance for the service water systemthrough the review of deficiencies identified, historical perform ance, and overall systemperformance. The following documents were reviewed:Work Order 0522187 - Detectable Leakage from 1-SW-V-127;Work Order 0615037 - Interim repair to the thinned area downstreamof SW-P-41B;Condition reports for the past year, selected items in detail;Service Water Maintenance Rule Performance & Scope Report; andMaintenance Rule performance data including maintenance rule function failuresand unavailability data.Based on issues identified in the review of the above documents, the inspectorsassessed: 1) the application for maintenance rule scoping and reliability/availabilityperformance criteria; 2) the corrective actions for deficient conditions; 3) the extent of condition reviews for common cause issues; and 4) the contribution of deficient work controls or work practices to any degraded conditions.The inspectors also reviewed the Seabrook UFSAR and TS for the two systems. Corrective actions and maintenance rule functional failure evaluations were assessed 9Enclosureagainst 10 CFR 50.65 requirements and against the guidance in Nuclear Managementand Resources Council (NUMARC) 93-01, "Industry Guideline for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants," Revision 2.
b. Findings
No findings of significance were identified.
1R13 Maintenance Risk Assessments and Emergent Work Evaluation (71111.13 -Five Samples)
a. Inspection Scope
The inspectors reviewed the scheduling and control for two planned maintenanceactivities and three emergent work troubleshooting activities in order to evaluate the effect on plant risk. The inspectors conducted interviews with operators, risk analysts, maintenance technicians, and engineers to assess their knowledge of the risk associated with the work, and to ensure that other equipment was properly protected. The inspectors evaluated the compensatory measures against Seabrook procedures, Maintenance Manual 4.14, "Troubleshooting," and Work Management Manual 10.1,"On-Line Maintenance." Specific risk assessments were conducted using Seabrook's "Safety Monitor." The inspectors reviewed the following items.On April 11 and 12, 2006, the inspectors reviewed troubleshooting effortsfollowing the control room receiving a Rod Control Non-Urgent Failure alarm.
The inspectors interviewed the engineers and the operators involved in the troubleshooting efforts. The inspectors also observed the troubleshooting activities and reviewed the MA 4.14 troubleshooting documentation.During the period of April 17 through April 20, 2006, the inspectors reviewedSeabrook's troubleshooting efforts following the control room receiving a DC Bus 11A ground alarm. The inspectors observed the troubleshooting efforts and interviewed the engineers and managers involved in the troubleshooting efforts.
The inspectors also reviewed the Plant Engineering Action Plan Register for the Bus 11A ground.On May 25, 2006, the inspectors reviewed the plant risk configuration duringplanned maintenance on a switchyard breaker, "B" atmospheric steam dump valve, "B" vital battery, and "B" emergency diesel generator. Seabrook's risk assessment, operators' ability to evaluate risk, and compensatory measurestaken to reduce risk were also evaluated.On June 1, 2006, the inspectors reviewed the plant risk configuration duringemergent activities associated with the "C" vital battery and a loop three delta temperature instrument. Work orders (WO) 0617387 and 0543214, troubleshooting activities, and Seabrook's risk assessment were also evaluated.
10EnclosureOn June 12, 2006, the inspectors reviewed the plant risk configuration duringplanned maintenance on a safety injection valve starter, several surveillancesidentified as potential trip initiators, and 6 of 12 condenser steam dump valves.
Seabrook's risk assessment and compensatory measures taken to reduce risk were evaluated.
b. Findings
No findings of significance were identified.
1R14 Personnel Performance Related to Non-Routine Plant Evolutions and Events (71111.14- Three Samples).1Untimely Operator Identification Results in Failure to Comply with TS 3.8.2
.1
a. Inspection Scope
The inspectors reviewed Seabrook's response to the "B" DC bus not being powered bya full capacity battery charger for approximately 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. The inspectors reviewed the applicable TS, the alarm response procedures, and NAP-402, "Conduct of Operations."
The inspectors interviewed licensed operators and operations department management.
The inspectors also examined Seabrook's immediate corrective actions for the failure to comply with TS 3.8.2.1.
b. Findings
Introduction.
Seabrook identified that the "B" DC Bus did not have a battery chargeraligned to it for approximately 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> which is greater than the two-hour allowed outage time as required by TS 3.8.2.1. This finding will be considered self-revealingsince two alarms were visible on the plants' video alarm system (VAS) from the time theevent occurred. This finding was determined to be of very low safety significance (Green) and was characterized to be an NCV for failure to comply with TS 3.8.2.1.Description. On June 21, 2006, the battery charger supply breaker was incorrectlyopened due to a maintenance technician error. This removed the required full capacity battery charger from the 125 volt DC "B" Bus. The opening of the battery charger supply breaker resulted in two control room VAS alarms. The operators failed to properly evaluate the VAS alarms on the evening of June 21, 2006, and did not recognize the degraded condition of thei 125 volt DC "B" Bus for the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. A new operating crew recognized the condition and determined that the plant was in atwo-hour TS shutdown action statement. Seabrook had been in a condition requiring the plant to enter TS action statement 3.8.2.1 from approximately 7:00 pm on June 21,2006, until 6:20 a.m. the next morning without entering the action statement. Theoperators coordinated with work control, engineering, and maintenance and were able to restore a full capacity battery charger to the "B" Bus within approximately 90 minutes of discovering the situation.
11EnclosureSeabrook performed several immediate corrective actions to ensure VAS alarms wouldbe properly addressed in a timely manner, including not treating any incoming alarms as expected regardless of the situation. These corrective actions were verified to have been implemented by the inspectors.The inspectors reviewed the control room logs and the alarm response for the two VASalarms received after the breaker was incorrectly opened. The inspectors interviewed operators, engineers, and managers. The inspectors compared the TS requirements to the actions taken by the first two shifts after the alarms were received in the control room and determined that the operator's failure to identify that 125 volt DC "B" Bus wasnot being supplied by a battery charger was a performance deficiency. This operator failure to identify resulted in exceeding the two-hour allowed outage time. Seabrook entered this issue into their corrective action program in CR 06-07045.Analysis. The finding was more than minor because it affected the Initiating Eventscornerstone objective to limit the likelihood of events that upset plant stability due tounreliable equipment performance. Using Appendix A, Phase 1 of MC 0609, the findingwas determined to be of very low safety significance (Green) since there had been an increase in the probability of an initiating event without an impact on mitigating systems,reactor coolant system leakage, or external event initiators. This conclusion was basedon the 125 Volt DC Battery remaining operable.This finding was associated with the cross-cutting area of human performance and theaspect of using human error prevention techniques since maintenance technicians opened the wrong breaker and the operators on two shifts did not identify and take the appropriate actions following the opening of the supply breaker from the battery charger to the 125 volt DC "B" Bus.Enforcement. Technical Specification 3.8.2.1.b., "DC Sources - Operating," requires inpart that the "B" Train include 125-volt Battery Bank 1B and that Bus 11B have a full capacity battery charger aligned to it. The Technical Specification limiting condition for operation action statement 3.8.2.1.b requires restoration of the battery charger tooperable status within two hours.Contrary to this requirement, between 6:58 p.m. on June 21, 2006, until 7:26 a.m. onJune 22, 2006, the 125 volt DC "B" Bus did not have an operable battery charger supplying it. This was a period of approximately 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> which exceeded the allowed outage time of two hours. Because this violation was of very low safety significance and Seabrook entered this finding into its corrective action program (CR 06-07045), this violation is being treated as an NCV consistent with Section VI.A.1 of the NRCEnforcement Policy (NCV 05000443/2006003-03, Untimely Operator IdentificationResults in Failure to Comply with TS 3.8.2.1)
.
12Enclosure.2Cooling Tower Basin Inspection
a. Inspection Scope
On April 13, 2006, Seabrook sent divers into the cooling tower basin to change out acolumn bolt in SW-P-110A along with inspecting the basin for any foreign materials that could interfere with the cooling tower system. Seabrook replaced the column bolt of theservice water pump to determine whether the bolt had degraded since the last inspection. The inspectors reviewed work orders (WO-0541278 and WO-01C3157)attended the pre-job briefing and observed the cooling tower inspection. The inspectors also interviewed the supervisor during the dive to verify procedural compliance.
b. Findings
No findings of significance were identified..3Operator Response to Loss of Enclosure Air Handling Fan
a. Inspection Scope
On June 3, 2006, the "B" enclosure air handling (EAH) fan, EAH-FN-31B, tripped due toa motor failure. Operators identified the tripped fan on June 4, 2006, approximately tenhours after the fan had tripped. Seabrook issued CR 06-06379 to investigate the cause of the fan failure and operator response. The inspectors examined operator response to the event, reviewed data logger alarms, and conducted a walkdown of the control room indications. The inspectors also reviewed the operator actions against the requirements in Seabrook administrative procedures and NRC requirements.
b. Findings
No findings of significance were identified.
1R15 Operability Evaluations (71111.15 - Six Samples)
a. Inspection Scope
The inspectors reviewed operability evaluations and/or condition reports in order toverify that the identified conditions did not adversely affect safety system operability orplant safety. The evaluations were reviewed using criteria specified in Generic Letter 91-18, "Resolution of Degraded and Nonconforming Conditions" and Inspection Manual Part 9900, "Operable/Operability - Ensuring the Function C apability of a System orComponent." In addition, where a component was determined to be inoperable, the inspectors verified the TS limiting condition for operation implications were properly addressed. The inspectors performed field walkdowns, interviewed personnel, and reviewed the following items:
13EnclosureCR 06-00953 and Deficiency Tag 50415 which identified a low air supplycondition to the "C" MSIV due to supply air bleeding through an unseated air motor shuttle valve. This condition was temporarily corrected by quickly isolating and unisolating both air supply trains to reseat the shuttle valve. If left uncorrected, this condition may have allowed the MSIV to drift closed.
Corrective actions to address the deficiency is planned using Work Order 0602982.CR 06-03866 evaluated the effects of debris found in the floor drain system ofthe Emergency Feedwater Pump House during floor drain inspections completed using WO 0545821. Seabrook evaluated the impact of an internal flood and the potential consequences. Seabrook determined under the design basis conditions (UFSAR 9.3.3 and TP7, "Seabrook Station Moderate Energy LineBreak Study," Revision 5) that a gap under an exterior door would remove sufficient water to prevent impact on safety-related equipment in the pump house. The inspectors reviewed the evaluation, compared the result with the design basis documents, and conducted a walkdown of the pump house to assess vulnerabilities to floods. This issue was also discussed in Section 1R06of this report.CR 06-03715 evaluated the effects of movement of the stuffing box journalsleeve on SW pumps 41 "C" and "D." Seabrook evaluated the potential impact on operability of the SW system and the extent-of-condition to other pumps withsimilar stuffing box set-ups. The inspectors reviewed the evaluation and interviewed the operators and engineers involved.CR 06-06234 evaluated the effects of a loop three delta temperature change thatresulted in a control room alarm. The inspectors reviewed the initial operabilityassessment and subsequent engineering evaluation of the impact of the 1.6 percent power change to the loop 3 delta temperature instrument.CR 06-06720 evaluated the effects of a discharge pressure control valve failureon the startup feedwater pump. The inspectors reviewed the degraded condition, conducted field walkdowns of the system, examined a similar previousissue (CR 03-05214), and evaluated compensatory actions.CR 06-06759 evaluated the effects of replacing the fan motor for the 31B fanwith a more powerful motor. The inspectors reviewed the design package and interviewed the engineers and mechanics involved in the modification.
b. Findings
No findings of significance were identified.
14Enclosure1R17Permanent Plant Modification (71111.17A - One Sample)
a. Inspection Scope
The inspectors reviewed the design change, MMOD 06-0534, "EAH-FN 31B MotorReplacement." This modification replaced an existing failed motor in a ventilation system with a new motor of different design and specifications. The inspectorsexamined the design qualifications of the new motor including the environmental and seismic qualifications, electrical and mechanical design differences, and modifications made to the exiting housing. Walkdowns of the new motor and the housing were completed to verify compliance with the design document. The inspectors also conducted interviews with engineers and maintenance technicians. The modification was evaluated against Seabrook procedures and NRC requirements.
b. Findings
No findings of significance were identified.
1R19 Post-Maintenance Testing (71111.19 - Eight Samples)
a. Inspection Scope
The inspectors reviewed post-maintenance testing (PMT) activities to ensure: 1) thePMT was appropriate for the scope of the maintenance work completed and in accordance with MA 3.5, "Post Maintenance Testing"; 2) the acceptance criteria were clear and demonstrated operability of the component; and 3) the PMT was performed inaccordance with procedures. The following PMT activities were reviewed:On April 14, 2006, for WO 0513721 following troubleshooting activities on apossible ground associated with a service water valve (1-SW-V-54). The inspectors interviewed the maintenance technicians and operators, reviewed the previous completed WO 0323103, and verified the testing was completed in accordance with the WO and OX1416.06, "Service Water Discharge Valves Quarterly Test and 18 Month Position Verification," Revision 5;On April 14, 2006, using OX1416.05, "Service Water Cooling Tower PumpsQuarterly and 2 Year Comprehensive Test," Revision 7, following maintenance on the "A" cooling tower pump;On April 18, 2006, for WO 0616426 following troubleshooting activities on aground on Bus 11A. The inspectors interviewed the operators and engineers, and reviewed the work package associated with WO 0616426;On April 24 and 26, 2006, for WO 0442810 following shaft replacement on the"A" essential switchgear supply fan; 15EnclosureOn May 1 through May 6, 2006, following completion of an 18-month overhaul ofthe "B" EDG. The inspectors reviewed the PMTs for 18 of the work orders. The work orders included preventive maintenance activities, corrective maintenance activities, and design modifications;On May 10 through May 12, 2006, for WO 0443930 following replacement of thebatteries for the reactor vessel level indication system. The inspectors interviewed the engineer and the instrument and controls technicians involved in the work;On June 10, 2006, for WO 0617586 following the installation of a new fan motoron EAH-FN-31B. The inspectors interviewed the engineers and maintenance technicians involved in the motor installation and testing; andOn June 21 and 22, 2006, for Work Order 0522187 and 0615037, followinginterim ASME Code repairs on the service water piping.
b. Findings
No findings of significance were identified.
1R22 Surveillance Testing (71111.22 - Six Samples)
a. Inspection Scope
The inspectors observed portions of surveillance testing activities of safety-relatedsystems to verify that t he system and components were capable of performing theirintended safety function, to verify operational readiness, and to ensure compliance with required Technical Specifications and surveillance procedures. The inspectors attended selected pre-evolution briefings, performed system and controlroom walkdowns, observed operators and technicians perform test evolutions, reviewed system parameters, and interview ed the system engineers and field operators. The testdata recorded was compared to procedural and technical specification requirements, and to prior tests to identify any adverse trends. The following surveillance procedureswere reviewed:On April 10, 2006, OX1406.02, "Containment Spray Pump and Valve QuarterlyOperability, 18 Month Position Indication and Comprehensive Pump Testing,"Revision 9;On May 11 and May 25, 2006, OX1406.04, "Service Water Quarterly Pump andDischarge Valve and Comprehensive Pump Testing," Revision 9 and OX1416.05, "Service Water Cooling Tower Pumps Quarterly and 2 Year Comprehensive Test," Revision 7;On May 19, 2006, RS0722, "New Fuel and Core Component Inspection,"Revision 7; 16EnclosureOn June 15, 2006, IX1680.921, "Solid State Protection System (SSPS) Train A -Actuation Logic Test," Revision 9;On June 29, 2006, LX0563.06, "Loss of Voltage Protection MonthlySurveillance," Revision 3, and LX0563.07, "Degraded Voltage Protection MonthlySurveillance," Revision 1.As a sixth sample, the inspectors reviewed the calibration and testing associated withfour instruments used to detect reactor coolant system leakage ("A" and "B"Containment Sump Level Indicators, 1-LD-L-8332 and1-LD-L-8333 and Radiation Monitors, 1-RM-R-6528 and 1-RM-R-6548. The last three calibrations were reviewed to identify trends and potential reliability issues. The inspectors also interviewedmaintenance personnel and the system engineer to assess any deficient conditions andto discuss the radiation monitor improvement plan. The Documents reviewed during the inspection are listed in the Attachment.
b. Findings
No findings of significance were identified.
1R23 Temporary Plant Modifications (71111.23 - Two Samples)
a. Inspection Scope
The inspectors reviewed temporary modifications (TMODs)06-002, 06-004, andassociated implementing documents to verify Seabrook's design basis and systemoperability were maintained. TMOD 06-002 was associated with a repair of a through-wall leak in a non-safety related section of the service water system that transfers theturbine building heat loads to the circulating water system.TMOD 06-004 was associated with the rod control cabinet computer alarms. The rodcontrol system non-urgent alarm was locked in due to a known and evaluated powersupply failure. The power supply was scheduled to be replaced during the next refueling outage. The modification was associated with the alarm circuitry bypassing the power supply failure and clearing the non-urgent alarm. The modification reduced the burden on the operators and prevented the problem from masking any future failures.The inspectors interviewed engineers and operators, completed field walkdowns, andreviewed the following documents:Maintenance Manual, MA 4.3A, "Temporary Modifications and TemporaryAlterations," Rev. 16;WO 0616449, Implementing document for Temporary Modification 06TMOD004;TMOD 06-002, Temporary Patch on SW Outfall Line to CW, Revision 1; andWO 0602161, Emergency Work Order to Repair Pipe Thru Wall Leak on ServiceWater Pipe.
17EnclosureThe inspectors verified that temporary modifications were completed in accordance with NRC requirements and plant procedures. The procedural requirements includedmodifications to plant drawings, tagging of plant equipment affected by modifications, and procedural changes. The inspectors verified 10 CFR 50.59 reviews and 10 CFR 50.65(a)(4) risk evaluations were completed correctly. The inspectors also examined the combined effect of the modification with the other outstanding temporary modifications.
b. Findings
No findings of significance were identified.
18EnclosureCornerstone: Emergency Preparedness (EP)1EP4Emergency Action Level and Emergency Plan (E-Plan) Changes
a. Inspection Scope
(IP
71114.04 - One Sample)During the period of September 2005 to March 2006, the NRC received changes madeto Seabrook's E-Plan in accordance with 10 CFR 50.54(q).
Seabrook determined the changes did not decrease the effectiveness of the E-Plan; and, also that the E-Plancontinued to meet the requirements of 10 CFR 50.47(b) and Appendix E to 10 CFR Part 50. A selected sample of E-Plan changes was reviewed in-office by the inspectors.
This review does not constitute approval of the changes and, as such, the changes and the associated 10 CFR 50.54(q) reviews are subject to future NRC inspection. The inspection was conducted in accordance with NRC Inspection Procedure 71114,Attachment 4.
d. Findings
No findings of significance were identified.2.RADIATION SAFETYCornerstone: Public Radiation Safety2PS2Radioactive Material Processing and Transportation (71122.02 - Six Samples)
a. Inspection Scope
During the period May 15 to 18, 2006, the inspectors conducted the following activitiesto verify that Seabrook's radioactive material processing and transportation programs complied with the requirements of 10 CFR 20, 61, and 71; and Department of Transportation (DOT) regulations 49 CFR 170-189.Radioactive Waste Systems WalkdownThe inspectors walked down accessible portions of the radioactive liquid processingsystems with the Senior Technical Specialist-RadWaste, on May 16, 2006. During thistour, the inspectors evaluated if the systems and facilities were consistent with thedescriptions contained in the UFSAR and the Process Control Program, evaluated the general material conditions of the systems and facilities, and identified any changes tothe systems. The inspectors evaluated recent changes made to liquid radwasteprocessing systems including their potential radiological impact, the current processes for transferring radioactive resin/sludge to shipping containers, and the subsequent de-watering process.
19EnclosureOn May 17, 2006, the inspectors walked down portions of candidate systems that are tobe retired in-place, with the system engineer, and discussed the status of administrativeand physical controls for these systems including components of the Boron RecoverySystem, Steam Generator Blowdown System, and Asphalt Solidification System. On May 16, 2006, the inspectors inspected various radioactive material storagelocations, with the Supervisor, Radiological Waste Services, including the Radioactive Materials Storage Building, the Unit 2 Cooling Tower, and seavans stored on site, to confirm that inventories were current, that material was properly labeled, and thatcontainers were in satisfactory material condition. Waste Characterization and ClassificationThe inspection included a review of the waste characterization and classificationprogram for regulatory compliance, including:*the radio-chemical sample analysis results for various radioactive waste streams,including spent resins, dry active waste, and mechanical filters;*the development of scaling factors for hard-to-detect radio-nuclides;
- methods and practices to detect changes in waste streams; and
- characterization and classification of waste relative to 10 CFR 61.55 and determination of a DOT shipment subtype per 49 CFR 173.Shipment PreparationThe inspection included a review of radioactive waste program records, shipmentpreparation procedures, and observations of in-progress activities for regulatory compliance, including:*Attending the pre-job briefing, and observing the transfer of a High IntegrityContainer, containing spent resin, to a shipping cask, and cask closure on May 15, 2006. The inspectors subsequently observed technicians performing vehicle radiation surveys on this shipment (Shipment No.06-015), on May 15, 2006. The inspectors confirmed that the shipping package was properly labeled and marked, and that the vehicle was properly placarded. The inspectors attended the driver's briefing and observed that the driver was provided emergency instructions and the proper shipping papers.*Observing technicians performing a transfer and de-watering of spent resin fromthe "A" Spent Resin Storage Tank to a High Integrity Container, on May 18, 2006. The inspectors attended the pre-job briefing, and observed the transfer and de-watering process to evaluate procedure compliance.*Reviewing radioactive material shipping logs for 2004, 2005, and 2006.
20Enclosure*Verifying compliance with the relevant Certificates of Compliance and relatedprocedures for in-use shipping casks.*Verifying that Seabrook had the most current amendment NRC (or agreementstate) license authorization for shipment recipients for seven shipments listed inthe shipping records section of this report.*Verifying that training was provided to appropriate personnel responsible forclassifying, handling, and shipping radioactive materials, in accordance with NRC Bulletin 79-19, and 49 CFR 172 Subpart H.Shipment RecordsThe inspectors selected and reviewed records associated with seven non-exceptedshipments of radioactive materials made since the last inspection of this area. The shipments were Nos.05-040,05-044, 05-056,05-059, 05-063,06-004, and 06-015. The following aspects of the radioactive waste packaging and shipping activities were reviewed:*implementation of applicable shipping requirements including proper completionof manifests;* implementation of specifications in applicable certificates-of-compliance, for theapproved shipping casks, including limits of package contents;* classification of radioactive materials relative to 10 CFR 61.55 and 49 CFR 173;
- labeling of containers relative to container dose rate;
- radiation and contamination surveys of packages;
- placarding of transport vehicles;
- conduct of vehicle checks;* providing of emergency instructions to the driver;
- completion of shipping papers; and
- notification by the recipient that the radioactive materials have been received.
b. Findings
No findings of significance were identified.
OTHER ACTIVITIES
4OA1Performance Indicator Verification (71151 - Six Samples)
a. Inspection Scope
The inspectors sampled Seabrook submittals for the performance indicators (PIs) listedbelow for the period from January 2004 through March 2006. To evaluate the accuracy of the PI data reported during that period, PI definitions and guidance contained in 21EnclosureNEI 99-02, "Regulatory Assessment Indicator Guideline," Revision 4 were used to verifythe basis in reporting for each data element.Initiating Events CornerstoneUnplanned Scrams per 7,000 Critical HoursUnplanned Scrams with Loss of Normal Heat RemovalUnplanned Power Changes per 7,000 Critical HoursMitigating Systems CornerstoneSafety System Functional FailuresBarrier Integrity Cornerstone Reactor Coolant System Specific ActivityReactor Coolant System (RCS) LeakageThe inspectors reviewed plant records such as Licensee Event Reports (LERs),operating logs, procedures, and interviewed applicable Seabrook personnel to verify the accuracy and completeness of Seabrook's PI data.The inspectors reviewed the PI data for reactor coolant system activity by verifying thecalculations and observing a reactor coolant system sample and analysis usingCS0910.01 and CX0901.02 (See Section 1R22, Surveillance Testing). The inspectorsreviewed the following documents in the evaluation of the PI data:JD0999.910, "Reporting Key Performance Indicators Per NEI 99-02," Revision 0;RCS sample results given in iodine 131 to 135 and as dose equivalent iodine; andTS 3.4.8, "Specific Activity."The inspectors reviewed the RCS leakage PI through a review of computer data fromApril 2004 through April 2006 and examination of ODI.63, "Operations Department KPI Maintenance Instruction, Revision 6 and OX1401.02, "RCS Steady State Leak RateCalculation," Revision 6. The inspectors also reviewed the Technical Specification required surveillance completed on leakage detection instrumentation (see 1R22).
b. Findings
No findings of significance were identified.4OA2Identification and Resolution of Problems (71152 - One Sample).1Routine Condition Report Screening
a. Inspection Scope
As required by Inspection Procedure 71152, "Identification and Resolution of Problems,"
22Enclosureand in order to help identify repetitive equipment failures or specific human performanceissues for follow-up, the inspectors performed a daily screening of items entered into the Seabrook's corrective action program. This review was accomplished by accessing Seabrook's computerized database.
b. Findings
No findings of significance were identified..2Semi-Annual Problem Identification and Resolution Trend Review
a. Inspection Scope
As required by Inspection Procedure 71152, Identification and Resolution of Problems,the inspectors performed a review of Seabrook's corrective action program and associated documents to identify trends that may indicate existence of more safety significant issues. The inspectors' review was focused on repetitive equipment and corrective maintenance issues but also considered the results of daily inspector corrective action program item screening discussed in Section 4OA2.1. The inspectors compared and contrasted their results with the results contained in Seabrook's Corrective Action Program Quarterly Trend Report. Corrective actions associated with a sample of the issues identified in the licensee's trend report were reviewed for adequacy.
b. Findings
No findings of significance were identified..3Radioactive Material Processing and Transportation
a. Inspection Scope
The inspectors reviewed the 2005 Annual Radioactive Effluent Release Report, elevenCondition Reports, a Quality Assurance Audit Report, and recent Seabrook Daily Quality Summary Reports relating to radioactive material control and shipping. Through this review, the inspectors assessed Seabrook's ability to identify problems, and thepromptness and effectiveness of the resulting corrective actions. This review was conducted against the criteria contained in 10 CFR 20.11(c), Technical Specifications, and licensee's procedures.
b. Findings
No findings of significance were identified.
23Enclosure.4Annual Sample: Operator Workaround Review
a. Inspection Scope
The inspectors reviewed Seabrook's current listing of operator workarounds andoperator burdens to determine whether the cumulative impact of the workarounds adversely impacted the ability of the operators to implement emergency procedures orrespond to plant transients. The inspectors examined NAP-402, "Conduct of Operations," Attachment K and "Operator Workarounds and Burdens," Revision 0, to verify that this procedure provided the necessary guidance to adequately address the cumulative effects the workarounds had on the operation, reliability, and availability ofaffected systems. The inspectors also reviewed selected CRs and quarterlyassessments completed under WOs 0521967 and 0532642. The items were verified to be properly tracked and scheduled for completion based on the priority and impact on the plant. The inspectors also examined one workaround in further detail to verify that correctiveactions were planned and compensatory actions were adequate. This workaround was associated with the ability of main feedwater isolation valves to reopen following closuredue to a feedwater isolation signal. The valves' safety function is to close in response to a feedwater isolation signal. Although not a credited safety-related function, thefeedwater isolation valves are described in the emergency operating procedure to re-establish flow to the steam generators in certain scenarios.
b. Findings and Observations
No findings of significance were identified. The inspectors determined that Seabrookappropriately identified, tracked, and corrected workaround and operator burdens. The periodic reviews for cumulative effects were completed and discreet acceptance criteria were met. During the detailed review of the feedwater isolation valve workaround, the inspectors identified a potential knowledge deficiency of the mitigating actions for a feedwater isolation valve's inability to reopen. The inspectors concluded that this issuewas of minor significance since two of the four feedwater isolation valves had already been upgraded and were no longer susceptible to the issue, the multiple licensed operators on each crew and in the technical support center would compensate for any knowledge deficiency, and the scenarios where the valves would be needed are beyond design basis with a very low likelihood of occurrence..5 Cross-Reference of Problem Identification and Resolution FindingsThe finding in Section 1R06.2, "Untimely Corrective Actions for Degraded Floor Drains,"was associated with the cross-cutting area of problem identification and resolution in that Seabrook failed to take appropriate corrective actions in a timely manner for the degraded floor drain systems in the plant after identifying the issue in 2000.
24EnclosureThe finding in Section 1R06.3, "Untimely Identification and Evaluation of DegradedHydrostatic Barriers," was associated with the cross-cutting area of problem identification and resolution in that Seabrook failed to thoroughly evaluate andimplement timely compensatory measures for the degraded hydrostatic barriers in the cable spreading room.4OA3Event FollowUp (71153 - One Sample).1(Closed) LER 50-443/06-002, Noncompliance with the Requirement of TechnicalSpecification 6.8.1.2.a.
a. Inspection Scope
On March 8, 2006, Seabrook discovered that the annual report on workers that receivedgreater than 100 mrem/year was not submitted by March 1, 2006, as required by TS 6.8.1.2.a. The inspectors reviewed the licensee event report, CR 05-02672, andcorrective actions to evaluate the accuracy of the licensee event report and to verify compliance with the reportability requirements in 10 CFR 50.73, NUREG 1022, "EventReporting Guidelines 10 CFR 50.72 and 50.73," Revision 2, and Facility OperatingLicense Condition 2.G. The corrective actions addressed the issue and provided measures to preclude repetition of the error. The error was an administrative issue and did not impact equipment at the plant. The failure to comply with TS 6.8.1.2.aconstitutes a violation of minor significance that is not subject to enforcement action in accordance with the NRC's enforcement policy.
b. Findings
No findings of significance were identified..2(Closed) URI 50-443/2006002-04, Degraded Cable Spreading Room Flood Seals andLER 50-443/2006-003, Voluntary LER for Deficient Hydrostatic BarriersThis issue was addressed in Section 1R06.3 and was documented as a non-citedviolation. The URI and the voluntary LER are closed.4OA5Other.1Implementation of Temporary Instruction (TI) 2515/165 - Operational Readiness of Offsite Power and Impact on Plant Risk
a. Inspection Scope
The objective of TI 2515/165, "Operational Readiness of Offsite Power and Impact on Plant Risk," was to gather information to support the assessment of nuclear power plant operational readiness of offsite power systems and impact on plant risk. The inspectorsevaluated Seabrook procedures against the specific offsite power, risk assessment and 25Enclosuresystem grid reliability requirements of TI 2515/165. The inspectors also discussed theattributes with licensee personnel. The information gathered while completing this TI was forwarded to the Office ofNuclear Reactor Regulation for further review and evaluation on April 3, 2006.
b. Findings
No findings of significance were identified.4OA6Meetings, including ExitExit Meeting SummaryThe inspectors presented the inspection results to Mr. G. St. Pierre on July 12, 2006,following the conclusion of the inspection period. The licensee acknowledged the findings presented. The licensee did not indicate that any of the information presentedat the exit meeting was proprietary.ATTACHMENT:
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee personnel
- M. Bianco, Radiological Waste Services Supervisor
- R. White, Security Manager
- R. Campione,Nuclear Oversight Supervisor
- W. Cox, Radiological Waste Services, Senior Technical Analyst
- P. Freeman, Engineering Director
- F. Hannify, Radiological Waste Services, Senior Technical Analyst
- P. Harvey, Chemistry Manager
- M. Kiley, Station Director
- M. Makowicz, Plant Engineering Manager
- D. Masters, Senior Component & Test Engineer
- M. O'Keefe, Regulatory Compliance Supervisor
- M. Ossing, Engineering Support Manager
- D. Ritter, Operations Manager
- V. Robertson, Regulatory Compliance Engineer
- D. Robinson, Chemistry Supervisor
- V. Sanchez, Senior Nuclear Analyst
- G. Shampy, Materials Manager
- D. Sherwin, Maintenance Manager
- T. Smith, Rad Technical Specialist (Training)
- G. St. Pierre, Site Vice President
- R. Thurlow, Radiation Protection Manager
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Closed:05000443/2006002LERNoncompliance with the Requirement of TechnicalSpecification 6.8.1.2.a. (Section 4OA3.1)05000443/2006002-04URIDegraded Cable Spreading Room Flood Seals(Section 4OA3.2)05000443/2006003LERVoluntary LER for Deficient Hydrostatic Barriers(Section 4OA3.2)
Opened and Closed
- 05000443/2006003-01NCVUntimely Corrective Actions for Degraded Floor Drains(Section 1R06.2)
A-2Attachment05000443/2006003-02NCVUntimely Identification and Evaluation of DegradedHydrostatic Barriers (Section 1R06.3)05000443/2006003-03NCVUntimely Operator Identification Results in Failure toComply with TS 3.8.2.1 (Section 1R14.1)
LIST OF DOCUMENTS REVIEWED
Section 1R06:
- Flood Protection Measures