IR 05000261/2008004
| ML083030287 | |
| Person / Time | |
|---|---|
| Site: | Robinson |
| Issue date: | 10/24/2008 |
| From: | Randy Musser NRC/RGN-II/DRP/RPB4 |
| To: | Walt T Carolina Power & Light Co |
| References | |
| IR-08-004 | |
| Download: ML083030287 (38) | |
Text
UNITED STATES NUCLEAR REGULATORY COMMISSION REGION II SAM NUNN ATLANTA FEDERAL CENTER 61 FORSYTH STREET, SW, SUITE 23T85 ATLANTA, GEORGIA 30303-8931 October 24, 2008
Carolina Power and Light Company ATTN: Mr. Tom Walt Vice President - Robinson Plant H. B. Robinson Steam Electric Plant Unit 2 3851 West Entrance Road Hartsville, SC 29550 SUBJECT: H.B. ROBINSON STEAM ELECTRIC PLANT - NRC INTEGRATED INSPECTION REPORT 05000261/2008004
Dear Mr. Walt:
On September 30, 2008, the US Nuclear Regulatory Commission (NRC) completed an inspection at your H.B. Robinson reactor facility. The enclosed integrated inspection report documents the inspection findings, which were discussed on September 25, with you and other members of your staff.
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
Based on the results of this inspection, the inspectors identified two issues of very low safety significance (Green).
Both of these issues were determined to involve violations of NRC requirements. However, because of their very low safety significance and because they have been entered into your corrective action program (CAP), the NRC is treating these issues as non-cited violations, in accordance with Section VI.A.1 of the NRC's Enforcement Policy. If you contest these non-cited violations, you should provide a response with the basis for your denial, within 30 days of the date of this inspection report to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555-0001, with copies to the Regional Administrator, Region II; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the H.B. Robinson facility.
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document CP&L 2 system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html http://www.nrc.gov/NRC/ADAMS/index.html.(the Public Electronic Reading Room).
Sincerely,
/RA/ Randall A. Musser, Chief Reactor Projects Branch 4 Division of Reactor Projects Docket No.: 50-261 License No.: DPR-23
Enclosure:
Inspection Report 05000261/2008004 w/Attachment: Supplemental Information
_________________________ X G SUNSI REVIEW COMPLETE GJW OFFICE RII:DRP RII:DRP RII:DRP RII:DRP RII:DRP SIGNATURE RCH2 by email EDM by email RAM GJW JGW1 by email NAME RHagar EMorris RMusser GWilson JWorosilo DATE 10/17/2008 10/17/2008 10/24/2008 10/22/2008 10/29/2008 10/ /2008 10/ /2008 E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO CP&L 3
REGION II==
Docket No: 50-261 License No: DPR-23 Report No: 005000261/2008004 Facility: H. B. Robinson Steam Electric Plant, Unit 2 Location: 3581 West Entrance Road Hartsville, SC 29550 Dates: July 1, 2008 - September 30, 2008 Inspectors: R. Hagar, Senior Resident Inspector E. Morris, Resident Inspector Approved by: R. Musser, Chief Reactor Projects Branch 4 Division of Reactor Projects
Enclosure
SUMMARY OF FINDINGS
IR 05000261/2008-004; Carolina Power and Light Company; on 7/1/2008-9/30/2008; H.B. Robinson Steam Electric Plant, Unit 2; Maintenance Risk Assessment and Emergent Work,
Post Maintenance Testing.
The report covered a three-month period of inspection by resident inspectors. Two violations were identified. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006.
A. NRC-Identified and Self-Revealing Findings
Cornerstone: Mitigating Systems
- Green.
The inspectors identified a Green non-cited violation (NCV) of 10 CFR 50.65(a)(4) for the failure on August 14 to adequately assess plant risk as Yellow after post-maintenance valve lineups failed to restore service water cooling to the B emergency diesel generator (EDG). As a result, the licensee incorrectly assumed that the B EDG was available to perform its safety function prior to performing a post maintenance test, and thereby performed an inadequate risk assessment which lowered plant risk from Yellow to Green status. As an immediate corrective action, the licensee implemented Operations Night Order 08-10 which required interim measures be performed to ensure that plant risk will not be downgraded until the component being returned to service has been proven to be available by performing a functional verification. The licensee also plans to proceduralize this interim measure into procedure OMM-048, Work Coordination and Risk Assessment. This issue was entered into the licensee's corrective action (CA) program for resolution.
This finding was more than minor and affected the Mitigating Systems Cornerstone, because it is similar to example 7.f of Inspection Manual Chapter (IMC) 0612, Appendix E, "Examples of Minor Issues". In example 7.f this finding meets the "Not minor if" criteria because if the licensee had correctly assessed the risk that may result from performing the maintenance activity of post-maintenance testing, that risk assessment would have placed the plant into a higher risk category (i.e. from Green to Yellow risk). The finding has a cross-cutting aspect in the area of Human Performance because the licensee did not ensure that complete and accurate procedures were available and adequate to assure nuclear safety, in that the licensee failed to provide clear guidance in procedure OMM-048, Work Coordination and Risk Assessment, for declaring equipment available as it relates to performing plant risk assessments. (H.2(c)) (Section 1R13)
- Green.
The inspectors identified a Green NCV of Technical Specification 5.4.1 for the failure on August 11 to maintain configuration control of the service water system for the B emergency diesel generator (EDG) when a service-water isolation valve to the EDG was closed outside of an approved process. The failure to maintain equipment configuration control of the closed service water isolation valve is contrary to Regulatory Guide 1.33 which requires the licensee to implement procedures affecting quality, which includes procedures maintaining equipment configuration control. This failure directly led to this valve remaining closed after the licensee electrically aligned the EDG for automatic start and declared it available on August 14. With this valve closed and the EDG aligned for auto-start, the EDG would have started without cooling water, rendering the EDG incapable of meeting its designed safety functions. As immediate corrective actions, the licensee performed a comprehensive valve and switch line-up on the EDG and issued an operations night order which required operators to perform certain interim measures when operating components without procedural guidance or clearance order control, to ensure that a positive means of control has been established. The licensee also plans to revise appropriate operating procedures to clarify requirements for performing valve and switch line-ups after maintenance activities. This issue was entered into the licensee CA program for resolution.
This finding was more than minor and affects the Mitigating Systems Cornerstone because it is similar to example 5.c of IMC 0612 Appendix E, "Examples of Minor Issues". In example 5.c, this finding meets the "Not minor if" criteria because although work was still in progress when the finding was identified, the licensee had already returned the EDG to service, in that the licensee had considered the EDG available and had electrically aligned the EDG to auto-start. The finding has a cross-cutting aspect in the area of Human Performance because the licensee did not appropriately coordinate work activities by incorporating actions to address the operational impact of work activities, in that the licensee did not coordinate the closure of SW-90 in a manner to track or restore this valve to its safety related position after maintenance activities were completed. (H.3(b)) (Section 1R19)
B. Licensee-Identified Violations
None.
REPORT DETAILS
Summary of Plant Status The unit began the inspection period at rated thermal power. On July 25, the licensee reduced reactor power to 99.5% to compensate for an intermittent problem involving main turbine controls. The unit operated at 99.5% until September 24, when power was reduced to 75 percent of full power in preparation to shutdown for refueling outage 25. On September 25, power was further reduced to shutdown the unit at 0000 on September 26 to begin the outage. The unit remained shutdown at the end of the inspection period.
REACTOR SAFETY
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity
1R01 Adverse Weather Protection
.1 Readiness for Impending Adverse Weather Condition - Extreme Heat
a. Inspection Scope
The inspectors performed a detailed review of the licensee's procedures and preparations for operating the facility during the periods of time when ambient outside temperature was high and the ultimate heat sink was experiencing elevated temperatures. The inspectors focused on plant-specific design features and implementation of the procedures for responding to or mitigating the effects of these conditions on the operation of the facility's service water system. Inspection activities included a review of the licensee's adverse weather procedures, daily monitoring of the off-normal environmental conditions, and that operator actions specified by plant specific procedures were appropriate to ensure operability of the facility's normal and emergency cooling systems. Documents reviewed are listed in the Attachment.
b. Findings
No findings of significance were identified.
.2 Readiness for Impending Adverse Weather Condition - High Winds
a. Inspection Scope
When Hurricane Hanna's path of travel predicted potential high winds for the site on September 6, the inspectors reviewed actions taken by the licensee in accordance with procedure OMM-021, Operation During Adverse Weather, prior to the onset of that weather, to ensure that the adverse weather conditions would neither initiate a plant event nor prevent any system, structure, or component from performing its design function. The inspectors reviewed the operator actions to verify that the desired results could be achieved. Documents reviewed are listed in the Attachment.
b. Findings
No findings of significance were identified.
1R04 Equipment Alignment
.1 Partial System Walkdowns
a. Inspection Scope
The inspectors performed the following three partial system walkdowns, while the indicated structures, systems, and/or components (SSCs) were out-of-service for maintenance and testing:
System Walked Down SSC Out of Service Date Inspected A & C charging trains B charging pump July 1 C safety injection pump A safety injection pump July 29 A emergency diesel generator B emergency diesel generator August 14 To evaluate the operability of the selected trains or systems under these conditions, the inspectors compared observed positions of valves, switches, and electrical power breakers to the procedures and drawings listed in the Attachment.
b. Findings
No findings of significance were identified.
.2 Complete System Walkdown
a. Inspection Scope
The inspectors conducted a detailed review of the alignment and condition of the auxiliary feedwater system to verify that the existing alignment of the system was consistent with the correct alignment. To determine the correct system alignment, the inspectors reviewed the procedures, drawings, and the Updated Final Safety Analysis Report (UFSAR) section listed in the Attachment. The inspectors also walked down the system. During the walkdown, the inspectors reviewed the following:
- Valves were correctly positioned and did not exhibit leakage that would impact the functions of any given valve.
- Electrical power was available as required.
- Major system components were correctly labeled, lubricated, cooled, ventilated, etc.
- Hangers and supports were correctly installed and functional.
- Essential support systems were operational.
- Ancillary equipment or debris did not interfere with system performance.
- Tagging clearances were appropriate.
- Valves were locked as required by the locked valve program.
The inspectors reviewed the documents listed in the Attachment to verify that the ability of the system to perform its functions could not be affected by outstanding design issues, temporary modifications, operator workarounds, adverse conditions, and other system-related issues tracked by the engineering department.
b. Findings
No findings of significance were identified.
1R05 Fire Protection
a. Inspection Scope
For the five areas identified below, the inspectors reviewed the control of transient combustible material and ignition sources, fire detection and suppression capabilities, fire barriers, and any related compensatory measures to verify that those items were consistent with UFSAR Section 9.5.1, Fire Protection System, and UFSAR Appendix 9.5.A, Fire Hazards
Analysis.
The inspectors walked down accessible portions of each area and reviewed results from related surveillance tests to verify that conditions in these areas were consistent with descriptions of the areas in the UFSAR. Documents reviewed are listed in the Attachment.
The following areas were inspected: Fire Zone Description 2 emergency diesel generator "A" room 26 main transformers 20 emergency switchgear room and electrical equipment area 8 boron injection tank room 19 cable spreading room The inspectors reviewed the following ARs associated with this area to verify that the licensee identified and implemented appropriate corrective actions:
- 249398, Nuclear condition report (NCR) not immediately initiated for improperly performed fire protection surveillance test OST-611-10
- 262758, Fire protection post-maintenance testing documentation issue
b. Findings
No findings of significance were identified.
1R06 Flood Protection Measures
a. Inspection Scope
Internal Flooding The inspectors walked down the component cooling water pump room and the A emergency diesel generator room to verify that each area configuration, features, and equipment functions were consistent with the descriptions and assumptions used in Calculation RNP-F/PSA-0009, Assessment of Internally Initiated Flooding Events. Those rooms were selected because they contain risk-significant SSCs which are susceptible to flooding from postulated pipe breaks. The inspectors also reviewed the operator actions credited in the analysis to verify that the desired results could be achieved using the plant procedures listed in the Attachment.
b. Findings
No findings of significance were identified.
1R07 Heat Sink Performance
a. Inspection Scope
The inspectors conducted a walkdown and reviewed operations data to verify that the residual heat removal (RHR) heat exchangers could perform their safety related functions. The inspectors reviewed documentation of licensee testing and Maintenance Rule data, and inspected the RHR heat exchangers for evidence of leaks. The inspectors also verified the RHR heat exchangers were oriented as depicted in plant drawings. Documents reviewed are listed in the Attachment.
To verify that the licensee identified and implemented appropriate corrective actions, the inspectors reviewed AR 188462188462 performance monitoring of some safety related heat exchangers is insufficient to detect some potential degradation mechanisms.
b. Findings
No findings of significance were identified.
1R11 Licensed Operator Requalification
a. Inspection Scope
On August 6, the inspectors observed licensed-operator performance during requalification simulator training for operations crew one, to verify that operator performance was consistent with expected operator performance as described in full scope scenario LOCT-Outage-3. This training tested the operators' ability to operate components from the control room, direct auxiliary operator actions, and determine the appropriate emergency action level classifications while responding to the failure of radiation monitor R-18 and reactor coolant system leakage resulting in a loss of coolant accident. The inspectors focused on clarity and formality of communication, the use of procedures, alarm response, control board manipulations, group dynamics, and supervisory oversight.
The inspectors observed the post-exercise critique to verify that the licensee identified deficiencies and discrepancies that occurred during the simulator training.
Documents reviewed are listed in the Attachment.
b. Findings
No findings of significance were identified.
1R12 Maintenance Effectiveness
a. Inspection Scope
The inspectors reviewed the two degraded SSC performance problems or conditions listed below to verify the appropriate handling of these performance problems or conditions in accordance with 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, and 10 CFR 50.65, Maintenance Rule. Documents reviewed are listed in the Attachment.
The problems/conditions and their corresponding action requests (ARs) were:
Performance Problem/Condition AR Trend in diaphragm leakage in valves in the chemical and volume control system 259032 Actuator for a hot-leg safety injection shutoff valve (SI-869) would not operate the valve 231092 During the reviews, the inspectors focused on the following:
- Appropriate work practices,
- Identifying and addressing common cause failures,
- Scoping in accordance with 10 CFR 50.65(b),
- Characterizing reliability issues (performance),
- Charging unavailability (performance),
- Trending key parameters (condition monitoring),
- 10 CFR 50.65(a)(1) or (a)(2) classification and reclassification, and
- Appropriateness of performance criteria for SSCs/functions classified (a)(2) and/or appropriateness and adequacy of goals and corrective actions for SSCs/functions classified (a)(1).
To verify that the licensee identified and implemented appropriate corrective actions, the inspectors reviewed AR 266844266844 diaphragm to body leak preventive maintenance run to failure class improvement.
b. Findings
No findings of significance were identified.
1R13 Maintenance Risk Assessments and Emergent Work Evaluation
a. Inspection Scope
For the five time periods listed below, the inspectors reviewed risk assessments and related activities to verify that the licensee performed adequate risk assessments and implemented appropriate risk-management actions when required by 10 CFR 50.65(a)(4). For emergent work, the inspectors also verified that any increase in risk was promptly assessed, and that appropriate risk-management actions were promptly implemented. Documents reviewed are listed in the Attachment. Those periods included the following:
- July 11 - July 17, including emergent work involving the C charging pump and the B AFW pump, which resulted in a Yellow risk condition
- July 28 - August 1, including emergent troubleshooting turbine governor valves, routine maintenance on safety injection pump A breaker, corrective maintenance on B coolant charging pump, and surveillance testing of reactor protection logic train A
- August 4 - August 8, including scheduled maintenance on the steam driven auxiliary feedwater pump which resulted in a Yellow risk condition
- August 11 - August 15, including scheduled maintenance on the B emergency diesel generator which resulted in a Yellow risk condition
- August 31 - September 6, including the approach of Tropical Storm Hanna and scheduled maintenance on the fire suppression water system which together resulted in a Yellow risk condition
b. Findings
Introduction:
The inspectors identified a Green non-cited violation of 10 CFR 50.65(a)(4) for the failure on August 14 to adequately assess plant risk as Yellow after post-maintenance valve lineups failed to restore service water cooling to the B EDG. As a result, the licensee incorrectly assumed that the B EDG was available to perform its safety function, and thereby performed an inadequate risk assessment which lowered plant risk from Yellow to Green status.
Description:
On August 14, after maintenance had been performed on the B EDG, the licensee removed the clearance and performed certain valve lineups to restore the diesel to service. At 1205, the licensee declared the B EDG available and performed a risk assessment that reduced plant risk from Yellow to Green. This assessment was based on the assumption that the EDG was able to perform its safety functions and no longer out-of-service. However, at 1236, as a result of inspector questioning, the licensee determined that the B EDG was in fact not available to perform its safety function because a service water isolation valve had not been returned to its required open position during the post-maintenance valve lineups. With this service water valve closed, all cooling water was isolated to the EDG and the EDG would have failed to provide its designed safety functions. Therefore, during the time between 1205 and 1236, as a result of the licensee's incorrect assumption that the B EDG was available, the licensee assessed plant risk as Green when the actual plant risk remained Yellow. This inadequate risk assessment constituted a performance deficiency with respect to 10 CFR 50.65(a)(4), which requires that before performing maintenance activities, including post maintenance testing, the licensee shall assess the increase to plant risk that may result from the proposed maintenance activities.
Analysis:
This finding was more than minor and affects the Mitigating Systems Cornerstone, because it is similar to example 7.f of IMC 0612, Appendix E, "Examples of Minor Issues". In example 7.f this finding meets the "Not minor if" criteria because if the licensee had correctly assessed the risk that may result from performing the maintenance activity of post-maintenance testing of the B EDG, that risk assessment would have placed the plant into a higher risk category (i.e. from Green to Yellow risk). The finding was screened for significance using IMC 0609, Attachment 4. Using that attachment, since this finding was an issue with the assessment and management of risk associated with maintenance activities and affects the Mitigating Systems Cornerstone, Table 3b - SDP Phase1 screening worksheet for Initiating Events, Mitigating Systems, and Barriers Cornerstones, question 5 directs evaluating this finding using IMC 0609, Appendix K, Maintenance Risk Assessment and Risk Management Significance Determination Process. In Appendix K, using Flowchart 1, this finding screened as Green because it was not related to Risk Management Actions only and the calculated Risk Deficit (1.3E-9) was less than 1.0E-6.
The finding has a cross-cutting aspect in the area of Human Performance because the licensee did not ensure that complete and accurate procedures were available and adequate to assure nuclear safety, in that the licensee failed to provide clear guidance in procedure OMM-048, Work Coordination and Risk Assessment, for declaring equipment available as it relates to performing plant risk assessments. (H.2(c))
Enforcement:
10 CFR 50.65(a)(4) requires, in part, that before performing maintenance activities, the licensee shall assess and manage the increase in risk that may result from the proposed maintenance activities. Contrary to the above, on August 14 and before performing the maintenance activity of post-maintenance testing of the B EDG, the licensee failed to assess the increase in risk that resulted from that proposed maintenance activity, in that the licensee failed to perform an adequate risk assessment by verifying the availability of the EDG prior to reducing plant risk from Yellow to Green. Because this finding was of very low safety significance and has been entered into the licensee's corrective action program as AR 291888291888 consistent with Section VI.A of the NRC Enforcement Policy, this violation is being treated as a non-cited violation, and is designated as NCV 05000261/2008004-01, "Failure to adequately assess risk when assuming availability prior to performing post maintenance testing."
1R15 Operability Evaluations
a. Inspection Scope
The inspectors reviewed the five operability determinations associated with the documents listed below. The inspectors assessed the accuracy of the evaluations, the use and control of any necessary compensatory measures, and compliance with the Technical Specification (TS). The inspectors verified that the operability determinations were made as specified by Procedure OPS-NGGC-1305, Operability Determinations. The inspectors compared the justifications provided in the determinations to the requirements from the TS, the UFSAR, and associated design-basis documents to verify that operability was properly justified and the subject components or systems remained available, such that no unrecognized increase in risk occurred:
- Work order 1288237, motor driven auxiliary feedwater pump "A" discharge flow indicator and controller capacitor replacement
- Work order 1387868, chemical volume control tank high/low level alarm requires replacement
- NCR 291412, failed service water liner at B emergency diesel generator cooler inlet
- NCR 293061, B emergency diesel generator room fire detectors failed to actuate during surveillance testing
- NCR 296027, B auxiliary feedwater pump flow controller, AFW-FIC-1425, ears to "D" clip are missing and "D" clip appears to have reduced effectiveness
Documents reviewed are listed in the Attachment.
To verify that the licensee identified and implemented appropriate corrective actions, the inspectors reviewed AR 276134276134 failure to enter technical specification limiting condition for operation action statement during motor-driven auxiliary feedwater maintenance.
b. Findings
No findings of significance were identified.
1R18 Plant Modifications
a. Inspection Scope
The inspectors reviewed the temporary modification described in Engineering Change 70590, reactor coolant pump B oil reservoir high level alarm setpoint change, to verify that the modification did not affect the safety functions of important safety systems, and to verify that the modification satisfied the requirements of Procedure EGR-NGGC-005, Engineering Change, and 10 CFR 50, Appendix B, Criterion III, Design Control.
Documents reviewed are listed in the Attachment.
b. Findings
No findings of significance were identified.
1R19 Post Maintenance Testing
a. Inspection Scope
For the six post-maintenance tests listed below, the inspectors witnessed the test and/or reviewed the test data to verify that test results adequately demonstrated restoration of the affected safety functions described in the UFSAR and TS. Documents reviewed are listed in the Attachment.
The following tests were witnessed/reviewed:
Test Procedure Title Related Maintenance Activity Date Inspected PIC-002 D/P Electronic Transmitter (4-20 mA Output) B train containment spray flow meter, FT-958B, power supply replacement. July 1 PIC-033 Auxiliary Feedwater Flow Indicating Controllers FIC-1424, FIC-1425, and FIC-6416 B auxiliary feedwater pump flow indicator and controller, FIC-1425, repair July 18 OST-101-3 [Chemical and Volume Control System] Component Test Charging Pump C C charging pump valve and fluid head assembly replacement July 22 OST-202 Steam Driven Auxiliary Feedwater System Component Test Steam driven auxiliary feedwater pump gauge calibration, check valve inspection, and valves inspections August 6 OP-604 Diesel Generators "A" and "B" Service water heat exchanger and pipe replacement, two year preventative maintenance inspections August 15 OST-401-2 [Emergency Diesel Generator] A Diesel Fuel Oil System Flow Test Emergency diesel generator A fuel oil transfer pump control switch relocated to the reactor/turbine gauge board August 25 The inspectors reviewed the following ARs associated with this area to verify that the licensee identified and implemented appropriate corrective actions:
- 280747, radiation monitor R-31 voltage not set per work order instructions during power supply replacement.
- 293177, engineering change 64319 post maintenance testing not scheduled in plan of the week
b. Findings
Introduction:
The inspectors identified a Green NCV of technical specification (TS) 5.4.1 for the failure on August 11 to maintain configuration control of the service water system for the B EDG when a service water isolation valve to the EDG was closed outside of an approved procedure. The failure to maintain equipment configuration control of the subject valve was contrary to Regulatory Guide 1.33 which requires the licensee to implement procedures affecting quality, which includes procedures maintaining equipment control. This failure directly resulted in this valve remaining closed after the licensee electrically aligned the EDG for automatic start and declared the EDG available on August 14. With this valve closed and the EDG aligned for auto-start, the EDG would have started without cooling water, rendering the EDG incapable of meeting its designed safety functions.
Description:
On August 11, while placing a clearance to enable scheduled maintenance to begin on the B EDG, the licensee discovered that the clearance boundaries did not provide adequate isolation of service water to that component. In response to this discovery, operations personnel verbally directed the closure of isolation valve SW-90 to provide an additional boundary to service water flow. In this situation, since the scheduled maintenance was expected to require several days, procedure OMM-001-11, Logkeeping, required, in part, that operations personnel enter SW-90 into the control-room log as an out-of-position component and install a corresponding caution tag on the valve. However, operations personnel did neither; as a result, SW-90 was closed but no corresponding control-room log entry was made, and no corresponding caution tag was installed. Consequently, on August 14, after the licensee completed the scheduled maintenance on the EDG and removed the associated clearance, the licensee electrically aligned the EDG for autostart and declared the EDG available while SW-90 remained closed. (With SW-90 closed, service water flow to the EDG was isolated.)
After this alignment and declaration and before the licensee completed the post-maintenance test of starting the B EDG using OP-604, the inspectors identified that SW-90 was closed and discussed that identification with involved operations personnel. As a result, operations personnel suspended their plans to complete the post-maintenance test until after they had completed a comprehensive verification of valve lineups.
The inspectors considered that operations personnel failure to comply with the configuration-control requirements of procedure OMM-001-11 after they closed SW-90 was a performance deficiency. To address this issue, the licensee initiated NCR 291863.
Analysis:
This finding is more than minor and affects the Mitigating Systems Cornerstone because it is similar to example 5.c of IMC 0612 Appendix E, "Examples of Minor Issues". In example 5.c, this finding meets the "Not minor if" criteria because although work was in progress, the licensee had returned the EDG to service, in that the licensee had declared the EDG available and had electrically aligned the EDG for auto-start when the finding was identified. The significance of the finding was evaluated using IMC 0609 Attachment 4. In accordance with Table 4a of Attachment 4, this finding screened as GREEN, because the finding was not a design or qualification deficiency confirmed to result in a loss of operability or functionality, did not represent a loss of system safety function, did not result in a loss of safety function for a single train for greater than the TS allowed outage time, did not result in a loss of safety function of one or more non-TS trains of equipment designated as risk-significant for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, and did not screen as potentially risk significant due to a seismic, flooding, or severe weather initiating event.
The finding has a cross-cutting aspect in the area of Human Performance because the licensee did not appropriately coordinate work activities by incorporating actions to address the operational impact of work activities, in that the licensee did not coordinate the closure of SW-90 in a manner to track or restore this valve to its safety-related position after maintenance activities were completed. (H.3(b))
Enforcement:
TS 5.4.1 requires that written procedures shall be established, implemented, and maintained covering applicable procedures recommended in RG 1.33, Revision 2, Appendix A, February 1978, which includes administrative procedures covering equipment control. Site Procedure OMM-001-11, Log keeping, requires that component manipulations that are not part of an approved procedure shall be entered as a component out of position entry in the component out of position log and if that component will remain out of its normal position past shift turnover, then a caution tag shall be installed. Contrary to the above, on August 11, when the licensee closed a service water isolation valve to the B EDG outside of an approved procedure, the licensee failed to enter the valve into the component out-of-position log. Furthermore, when the service water valve remained out of its normal position past shift turnover, the licensee failed to install a caution tag on the valve. This resulted in failure to properly align the EDG for start-up on August 14, in that service water remained isolated to the EDG after the licensee aligned the diesel for automatic start and declared the EDG available for use. Because this finding was of very low safety significance and has been entered into the CAP as AR 291863291863and consistent with Section VI.A.1 of the NRC Enforcement Policy, this violation is being treated as a non-cited violation, NCV 05000261/2008004-02, Failure to maintain emergency diesel generator service water valve configuration control.
1R20 Refueling and Outage Activities
For the outage that began on September 26, the inspectors evaluated licensee outage activities as described below to verify that licensees considered risk in developing outage schedules, adhered to administrative risk reduction methodologies they developed to control plant configuration, and adhered to operating license and technical specification requirements that maintained defense-in-depth. The inspectors also verified that the licensee developed mitigation strategies for losses of the following key safety functions:
- inventory control
- power availability
- reactivity control
- containment Documents reviewed are listed in the Attachment.
.1 Review of Outage Plan
a. Inspection Scope
Prior to the outage, the inspectors reviewed the outage risk control plan to verify that the licensee had performed adequate risk assessments, and had implemented appropriate risk-management strategies when required by 10 CFR 50.65(a)(4).
b. Findings
No findings of significance were identified.
.2 Monitoring of Shutdown Activities
a. Inspection Scope
The inspectors observed portions of the cooldown process to verify that technical specification cooldown restrictions were followed.
b. Findings
No findings of significance were identified.
.3 Licensee Control of Outage Activities
a. Inspection Scope
During the outage, the inspectors observed the items or activities described below to verify that the licensee maintained defense-in-depth commensurate with the outage risk-control plan for key safety functions and applicable technical specifications when taking equipment out of service.
- Clearance Activities
- Reactor Coolant System Instrumentation
- Electrical Power
- Spent Fuel Pool Cooling
- Inventory Control
- Reactivity Control
- Containment Closure The inspectors also reviewed responses to emergent work and unexpected conditions to verify that resulting configuration changes were controlled in accordance with the outage risk control plan, and to verify that control-room operators were kept cognizant of the plant configuration.
b. Findings
No findings of significance were identified.
.4 Identification and Resolution of Problems
a. Inspection Scope
Periodically, the inspectors reviewed the items that had been entered into the CAP to verify that the licensee had identified problems related to outage activities at an appropriate threshold and had entered them into the corrective action program.
b. Findings
No findings of significance were identified.
1R22 Surveillance Testing
a. Inspection Scope
For the six surveillance tests listed below, the inspectors witnessed testing and/or reviewed the test data to verify that the systems, structures, and components involved in these tests satisfied the requirements described in the TS, the UFSAR, and applicable licensee procedures, and that the tests demonstrated that the SSCs were capable of performing their intended safety functions. Documents reviewed are listed in the Attachment.
Test Procedure Title Date Inspected OST-051* Reactor Coolant System Leakage Evaluation July 11 OST-201-2 [Motor Driven Auxiliary Feedwater Pump] System Component Train Test - Train B July 18 MST-020 Reactor Protection Logic Train "A" At Power July 30 EST-002 Power Distribution Measurement (Monthly Interval) August 5 OST-908 Component Cooling System Component Test August 21 OST-302-1** Service Water Pumps A & B Inservice Test August 28
- This procedure was a Reactor Coolant System leakage detection surveillance. **This procedure included inservice testing requirements.
The inspectors reviewed the following ARs associated with this area to verify that the licensee identified and implemented appropriate corrective actions:
- 286999, wrong gauge installed - discovered during surveillance testing
- 293061, B emergency diesel generator room fire detectors failed to actuate during surveillance testing
b. Findings
No findings of significance were identified.
Cornerstone: Emergency Preparedness
1EP6 Drill Evaluation
a. Inspection Scope
On July 15, the inspectors observed an emergency preparedness training evolution to verify licensee self-assessment of classification, notification, and protective action recommendation development in accordance with 10 CFR 50, Appendix E. The inspectors also attended the post-drill critique to verify that the licensee properly identified failures in classification, notification and protective action recommendation development activities. Documents reviewed are listed in the Attachment.
b. Findings
No findings of significance were identified.
OTHER ACTIVITIES
4OA1 Performance Indicator (PI) Verification
a. Inspection Scope
The inspectors verified the two PIs identified below. For each PI, the inspectors verified the accuracy of the PI data that had been previously reported to the NRC by comparing those data to the actual data, as described below. The inspectors also compared the licensee's basis in reporting each data element to the PI definitions and guidance contained in NEI 99-02, "Regulatory Assessment Indicator Guideline," Rev. 4. In addition, the inspectors interviewed licensee personnel associated with collecting, evaluating, and distributing these data.
Mitigating Systems Cornerstone
- Mitigating Systems Performance Index, Emergency AC Power
- Mitigating Systems Performance Index, High Pressure Safety Injection For the period from the second quarter of 2007 through the second quarter of 2008, the inspectors reviewed Licensee Event Reports (LERs), records of inoperable equipment, and Maintenance Rule records to verify that the licensee had accurately accounted for unavailability hours that the subject systems had experienced during the subject period. The inspectors also reviewed the number of hours those systems were required to be available and the licensee's basis for identifying unavailability hours.
b. Findings
No findings of significance were identified.
4OA2 Identification and Resolution of Problems
.1 Routine Review of ARs
To aid in the identification of repetitive equipment failures or specific human performance issues for followup, the inspectors performed frequent screenings of items entered into the CAP. The review was accomplished by reviewing daily AR reports.
.2 Annual Sample Review
a. Inspection Scope
The inspectors selected the following AR's for detailed review.
- 270087, battery charger engineering change and work order not followed as written. The inspectors selected this AR because it relates generally to the Mitigating Systems Cornerstone.
- 203620, pressure control valve for seal water to feedwater pump does not operate properly at low power requiring manual action to control seal water pressure. The inspectors selected this AR because it relates specifically to an operator workaround.
The inspectors reviewed these AR's to verify:
- complete and accurate identification of the problem in a timely manner;
- evaluation and disposition of performance issues;
- evaluation and disposition of operability and reportability issues;
- consideration of extent of condition, generic implications, common cause, and previous occurrences;
- appropriate classification and prioritization of the problem;
- identification of root and contributing causes of the problem;
- identification of corrective actions which were appropriately focused to correct the problem; and
- completion of corrective actions in a timely manner.
The inspectors also reviewed these AR's to verify compliance with the requirements of the CAP as delineated in Procedure CAP-NGGC-0200, Corrective Action Program, and 10 CFR 50, Appendix B. Documents reviewed are listed in the Attachment.
b. Observations and Findings
No findings of significance were identified.
4OA3 Event Follow-up
.1 Unexpected Repositioning of Turbine Control Valves
a. Inspection Scope
On July 24, turbine control valve GV2 unexpectedly repositioned open, causing steam flow and reactor power to increase. Before a significant plant transient occurred, control-room operators took manual control of turbine control valve positions to restore steam flow and reactor power to appropriate values. The inspectors reviewed the circumstances associated with that event to:
determine whether the event posed an actual or potential hazard to public health and safety, property, or the environment, as defined in NRC Management Directive 8.3, NRC Incident Investigation Program; verify that the control-room operators' response to the event was appropriate and in accordance with procedures and training; and verify that the licensee determined and adequately addressed the cause of the event.
Documents reviewed are listed in the Attachment.
b. Findings
No findings of significance were identified.
4OA5 Other Activities
.1 Quarterly Resident Inspector Observations of Security Personnel and Activities
a. Inspection Scope
During the inspection period, the inspectors conducted the following observations of security force personnel and activities to ensure that the activities were consistent with licensee security procedures and regulatory requirements relating to nuclear plant security. These observations took place during both normal and off-normal plant working hours.
These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples. Rather, they were considered an integral part of the inspectors' normal plant status review and inspection activities.
b. Findings
No findings of significance were indentified.
.2 Periodic Resident Inspector Review of INPO Evaluations
The inspectors reviewed the interim report of the Institute of Nuclear Power Operations (INPO) 2008 evaluation that was completed on April 18, 2008. The inspectors reviewed the report to ensure that issues identified were consistent with the NRC perspective of licensee performance and to verify if any significant safety issues were identified that required further NRC follow-up.
.3 (Open) Temporary Instruction (TI) 2515/176, Emergency Diesel Generator Technical Specification Surveillance Requirements Regarding Endurance and Margin Testing
a. Inspection Scope
The objective of this TI was to gather information to assess the adequacy of nuclear power plant EDG endurance and margin testing as prescribed by plant-specific TS. The inspector interfaced with the appropriate station staff to obtain the information specified in Attachment 1 of the TI-176 Worksheet. The TI applies to all operating nuclear power reactor licensees that use EDGs as the onsite standby power supply. The inspector verified the accuracy of the information by review of TS, EDG Design Basis Event (DBE) loading calculations, EDG endurance run test procedures, test data from the last three endurance tests performed on each EDG, EDG ratings, and EDG operating history. The information gathered will be forwarded to Nuclear Reactor Regulation/Division of Engineering/Electrical Engineering Branch (NRR/DE/EEEB) for further review to assess the adequacy and consistency of EDG testing at nuclear stations.
b. Findings and Observations
The TI is presently scheduled to be open until August 31, 2009, pending completion of the NRR/DE/EEEB review.
.4 (Closed) Operator Experience Smart Sample (OpEss) FY 2007-03, Crane and Heavy Lift Inspection, Supplemental Guidance
The inspectors completed their review of Operator Experience Smart Sample OpEss FY2007-03, Crane and Heavy Lift Inspection. The licensee has completed their load drop analysis and it is documented in calculation RNP-C/STRIU-1260. The load drop analysis does bound the maximum lifting heights and weights. The licensee has submitted a licensing document change request to update their FSAR with the summary description of the safety basis used for heavy load movements. The licensee plans to submit the change with the NRC within six months after the end of their fall outage.
4OA6 Meetings, Including Exit
On September 25, the resident inspectors presented the inspection results to Mr. T. Walt and other members of his staff. The inspectors confirmed that proprietary information was not provided or examined during the inspection.
- Supplemental Information
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee personnel
- C. Baucom, Manager, Support Services - Nuclear
- W. Farmer, Engineering Manager
- J. Huegel, Maintenance Manager
- E. Kapopoulos, Plant General Manager
- J. Lucas, Nuclear Assurance Manager
- J. Rhodes, Acting Radiation Protection Superintendent
- K. Jones, Operations Manager
- T. Walt, Vice President
- S. Wheeler, Supervisor, Emergency Preparedness
NRC personnel
- R. Musser, Chief, Reactor Projects Branch 4
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened
2515/176 TI Emergency Diesel Generator Technical Specification Surveillance Requirements Regarding Endurance and Margin Testing
Closed
None Opened &
Closed
- 05000261/2008004-01 NCV Failure to adequately assess risk when assuming availability prior to performing post maintenance
testing. (1R13)
- 05000261/2008004-02 NCV Failure to maintain emergency diesel generator service water valve configuration control. (1R19)
Previous Items
Closed
None
Discussed
None