ML18052B448

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Responds to NRC 871217 Ltr Re Violations Noted in Insp Rept 50-255/87-29.Corrective Actions:Technical Review of Procedure MO-29 Completed & Event Reviewed W/All on-shift Operations Personnel & Checklists Revised
ML18052B448
Person / Time
Site: Palisades Entergy icon.png
Issue date: 01/15/1988
From: Berry K
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
To:
NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM)
References
NUDOCS 8801210206
Download: ML18052B448 (3)


See also: IR 05000255/1987029

Text

I -* General Offices: 1945 West Parnell Road, Jackson, Ml 49201 * (517) 788-1636 January 15, 1988 Nuclear Regulatory

Commission

Document Control Desk Washington, DC 20555 DOCKET 50-255 -LICENSE DPR-20 -PALISADES

PLANT -RESPONSE TO INSPECTION

REPORT 87-029 Kenneth W Be..,Y Director Nuclear Licensing

NRC Inspection

Report 87-029 dated December 17, 1987 transmitted

one Notice of Violation

and requested

a written response.

The violation

involves the failure to comply with a written procedure

governing

the performance

of containment

isolation

valve position checks. Consumers

Power Company's

reponse to this violation

is as follows: Response:

Violation

(255/87029-01) (DPR) As .a result of the inspection

conducted

on November 3 through December 1, 1987 and in accordance

with the General Policy and Procedures

for NRC Enforcement

Actions (lOCFR Part 2, Appendix C), the following

violation

was identified:

Technical

Specification

6.8.1 requires the implementation

of certain procedures

including

those governing

the operation

of the Plant systems. Included in the procedures

governing

operation

of the Plant systems is Administrative

Procedure

4.02 which requires that when a valve " *** position is found to be different

from that specified, the Shift Supervisor

shall be notified and he shall authorize

the positioning

of the valve." Contrary to the above, on November 16, 1987 valve WGS-511 was found in a position (locked closed) contrary to Procedure

M0-29 requirements (Open); seven of the nine previous valve position checks performed

during 1986 and 1987 failed to identify and document the position discrepancy

and failed to report same to the Shift Supervisor.

8801210206

880115 PDR ADOCK 05000255 Q PDR OC0188-0011-NL04

..... -J.. * * * Nuclear Regulatory

Commission

PalisaQ.es

Plant Response to Inspection

Report 87-029 January 15, 1988 Corrective

Actions Taken And Results Achieved 2 On November 16, 1987, Plant Auxiliary

Operator performing

Technical cation Surveillance

Procedure

M0-29, "Engineered

Safety System Alignment", identified

a discrepancy/typographical

error regarding

the positioning

of containment

ventilation

header test valve, MV-WGS511.

The valve was found to be in its required locked closed position, however, M0-29 specifies

that the valve should be verified to be in the open position.

This procedural

discrepancy

had also been identified

during the second performance

of M0-29 in 1986. However, due to the Plant Review Committee (PRC) rejection

of a temporary

change to the procedure

and mis-communication

between Plant personnel, the procedure

was not corrected.

This procedure

has been performed

nine times since the error was identified

in 1986. As stated in the inspection

report, Consumers

Power and the NRC Senior Resident Inspector

believe that, the one inch test line valve which was found locked closed and capped was being verified*

as locked closed and the checklist

was being initialed

erroneously.

On November 18, 1987, a technical

review of procedure

M0-29 was completed.

This review entailed verifying

all other"valve

positions

indicated

within the procedure

were correct and then physically

verifying

that actual in-plant valve positions

corresponded

to their required positions.

No additional

errors were found in the procedure

or with valve positions.

The Plant Operations

Superintendent

then reviewed the event with all on-shift Operations

personnel.

On December 1, 1987, personnel

involved with the communication

error which resulted in the failure to correct the procedural

discrepancy

were counselled

with respect to the need to properly documenting

the closure of open PRC items. Temporary

changes to procedures

that are disapproved

by the PRC will be forwarded

to the originator

and the affected department

supervisor

to assure the procedural

error is otherwise

corrected

in a timely manner. Corrective

Actions To Be Taken To Avoid Further Noncompliance

Operations

Department

checklists

are being revised to ensure the following

exists: -Standardized

formatting

-All required valve positions

are fully printed out, no abbreviations

-Valves in potentially

contaminated

areas are arranged by rooms, with no two areas on the same sheet -A comment section is present on each sheet In addition, the above revisions

are also being performed

for all surveillance

procedures

containing

valve checklists.

OC0188-0011-NL04

Nuclear Regulatory

Commission

Palisades

Plant Response to Inspection

Report 87-029 January 15, 1988 An evaluation

is being conducted, to determine

the best way to assure that no discrepancies

exist before procedure

issuance.

Auxiliary

Operators

will be to be required to utilize original checklists

or procedures

during their performance.

Guidance has been provided to the Operations

Department

by the Radiological

Services Department

to provide expeditious

copying of contaminated

original checklists

or procedures.

Date When Full Compliance

Will Be Achieved All corrective

actions described

above, with the exception

of Surveillance

Procedure

revisions, will be completed

by June 1, 1988. Completion

of the Surveillance

Procedure

revisions

will occur by December 31, 1988 due to the extensive

number of Technical-Specifications

procedure

revisions

to be.done. Kenneth W Berry Director, Nuclear Licensing

-CC Administrator, Region III, NRC NRC Resident Inspector

-Palisades

OC0188-0011-NL04

3