ML17306A730

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Responds to NRC 920407 Ltr Re Violations Noted in Insp Rept 50-528/92-05 on 920126-0229.Corrective Actions:Hydrogen Test Bottles,Filled by Local Vendor,Removed from Svc,Quarantined & Returned to Vendor & Condition Rept Initiated
ML17306A730
Person / Time
Site: Palo Verde Arizona Public Service icon.png
Issue date: 05/14/1992
From: CONWAY W F
ARIZONA PUBLIC SERVICE CO. (FORMERLY ARIZONA NUCLEAR
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
102-02147-WFC-T, 102-2147-WFC-T, NUDOCS 9205200206
Download: ML17306A730 (31)


See also: IR 05000528/1992005

Text

ACCELERATED

DISTRIBUTION

DEMONSTPA.TION

SYSTEM REGULATORY

INFORMATION

DISTRIBUTION

SYSTEM (RIDS)ESSION NBR:9205200206

DOC.DATE: 92/05/14 NOTARIZED:

NO'OCKET Lij'IL:STN-50-528

Palo Verde Nuclear Station, Unit 1, Arizona Publi 05000528 AUTH.NAME AUTHOR AFFILIATION

CONWAY,W.F.

Arizona Public Service Co.(formerly Arizona Nuclear Power RECIP.NAME

RECIPIENT AFFILIATION

Document Control Branch (Document Control Desk)SUBJECT: Responds to NRC 920407 ltr re violations

noted in Insp Rept 50-528/92-05

on 920126-0229.Corrective

actions:hydrogen

test bottles, filled by local vendor, removed from svc,quarantined

&returned to vendor&condition rept initiated.

DISTRIBUTION

CODE IEOID COPIES RECEIVED LTR,L ENCL/SIZE'TITLE: General (50 Dkt)-Insp Rept/Notice

of Violation Response D NOTES:STANDARDIZED

PLANT 05000528 RECIPIENT ID CODE/NAME PD5 PD THOMPSON,M

INTERNAL: ACRS AEOD/DEIIB

DEDRO t NRR/DLPQ/LHFBPT

NRR/DOEA/OEAB

NRR/DST/DIR

8E2 NUDOCS-ABSTRACT

OGC/HDS1 RGN5 FILE 01 EXTERNAL: EG&G/BRYCE,J.H.

NSIC COPIES LTTR ENCL 1 1 1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 RECIPIENT ID CODE/NAME TRAMMELL, C AEOD AEOD/DSP/TPAB

NRR MORISSEAU,D

NRR/DLPQ/LPEB10

NRR/DREP/PEPB9H

NRR/PMAS/ILRB12

O~EG FILE 02 NRC PDR COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 D D R D NOTE TO ALL"RIDS" RECIPIENTS:

D D P LEASE HELP US TO REDUCE WASTE!CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT.20079)TO ELIMINATE YOUR NAhIE FROM DISTRIBUTION

LISTS FOR DOCUMENTS YOU DON'T NEED!TAL NUMBER OF COPIES REQUIRED: LTTR 24 ENCL 24

WILLIAM F.CONWAY EXECUTNEVICEPRESLDENT

NUCLEAR Arizona Public Service Company P.O.BOX 53999~PHOENIX.ARIZONA 85072-3999

102-02147-WFC/TRB/JRB

May 14, 1992 U.S.Nuclear Regulatory

Commission

Attention:

Document Control Desk Mail Station: P1-37 Washington, DC 20555 Reference:

Letter dated April 7, 1992, from S.A.Richards, Chief, Reactor Projects Branch, NRC, to W.F.Conway, Executive Vice President, Nuclear, Arizona Public Service Company.Gentlemen:

Subject: PALO VERDE NUCLEAR GENERATING

STATION (PVNGS)UNITS 1, 2 AND 3 REPLY TO NOTICE OF VIOLATIONS

50-528/92-05-01, 50-528/92-05-02

AND 50-528/92-05;03

File: 92-070-026

Arizona Public Service Company (APS)has reviewed NRC Inspection

Report 50-528, 529, 530/92-05 and the Notice of Violations

dated April 7, 1992.Pursuant to the provisions

of 10 CFR 2.201, APS'esponse

is attached.Appendix A to this letter is a restatement

of the Notice of Violations.

APS'esponse

is provided in Attachment

1.Per telephone conversation

on May 6, 1992, between H.J.Wong, NRC, and T.R.Bradish, APS, an extension of the due date for this response from May 7, 1992, to May 15, 1992.This extension was necessary as a result of PVNGS Unit 3 being in an ALERT emergency classification

from May 4, 1992, through May 6, 1992.Should you have any questions regarding this response, please contact me.Sincerely,'0 WFC/TRB/JRB/dmn

Attachments

1.Appendix A-Restatement

of Notice of Violations

2.Attachment

1-Reply to Notice of Violations

cc: J.B.Martin A i-i C'.nn 9205200206

920514 PDR ADDCK 05000528 8 PDR p7p,~)stI r Iiq5

'

APPENDIX A RESTATEMENT

OF NOTICE OF VIOLATIONS

50-528/92-05-02, 50-528/92-05-01

AND 50-528/92-05-03

NRC INSPECTION

CONDUCTED JANUARY 26, 1992-FEBRUARY 29)1992 INSPECTION

REPORT NOS.50-528, 529, AND 530/92-05

i

RESTATEMENT

OF NOTICE OF VIOLATIONS

50-528 92-05-02 50-528 92-0541 AND 50-528 92-05-03 During an NRC inspection

conducted on January 26 through February 29, 1992, three violations

of NRC requirements

were identified.

In accordance

with the"General Statement of Policy and Procedure for NRC Enforcement

Action," 10 CFR Part 2, Appendix C, the violations

are listed below: A.Unit 1 Technical Specification 6.8.1 states, in part, that written procedures

shall be established, implemented, and maintained

covering the activities

recommended

in Appendix A of Regulatory

Guide 1.33, Revision 2, February, 1978.Regulatory

Guide 1.33, Revision 2, Appendix A, recommends

surveillance

procedures

and general plant operating procedures.

Surveillance

procedure 36ST-9SB02,"PPS Bistable Trip Units Functional

Test," Step 8.11.6.2, requires the test performer to"ensure LO SG2 PRESS Trip Setpoint (Parameter

12)is at the MAXIMUM VALUE when in Mode 1 or 2.Adjust as necessary." Contrary to the above, on February 4, 1992, when performing

step 8.11.6.2, the test performer failed to ensure the LO SG2 PRESS trip setpoint (parameter

12)was at the maximum value when the unit was in Mode 1, resulting in the setpoint being approximately

50 pounds per square inch less that[sic]the minimum value allowed by Technical Specifications 2.2.1 and 3.3.2.2.General operating procedure 40DP-90P05,"Control Room Data Sheet Instructions," Step 2.3.2, requires that a reactor operator report"any abnormal and/or unusual condition" while filling out the Control Room Data Sheets.Contrary to the above, on February 4, 1992, at 5:00 pm, while filling out the Control Room Data Sheets, the reactor operator failed to note that the 42 steam generator low pressure setpoint was incorrectly

set.This is a Severity Level IV Violation (Supplement

I)applicable

to Unit 1.B.Unit 1 Technical Specification 6.8.1 states, in part, that written procedures

shall be established, implemented, and maintained

covering the applicable

procedures

recommended

in Appendix A of Regulatory

Guide 1.33, Revision 2, February 1978.Page 1

Regulatory

Guide 1.33, Appendix A;recommends

procedures

for performing

maintenance

and states that maintenance

that can affect the performance

of safety-related

equipment should be properly preplanned

and performed in accordance

with written procedures, documented

instructions, or drawings appropriate

to the circumstances.

Licensee Procedure 36MT-9RI06,'VNhdrawal

of ICI Cables," Section 8.4.5, requires the control element assembly (CEA)hoist to be used when withdrawing

fixed incore instruments (ICls)for refueling operations.

Contrary to the above, on February 25, 1992, the licensee failed to implement Procedure 36MT-9RI06, in that fixed ICI 455 was manually withdrawn without using the CEA hoist.This is a Severity Level IV violation (Supplement

I)applicable

to Unit 1.C.10 CFR 50, Appendix B, Criterion XII, requires that measures be established

to assure that tools, gages, instruments, and other measuring and testing devices used in activities

affecting quality are properly controlled, calibrated, and adjusted at specified periods to maintain accuracy within necessary limits.Contrary to the above, no measures were established

to assure that calibration

gas used for performance

of containment

hydrogen monitor surveillance

tests, an activity affecting quality, was properly controlled

and calibrated.

Specifically, on February 11, 1992, the Unit 2 Containment

Hydrogen Monitor Channel A surveillance

test (Procedure

36ST-9HP03)

was performed using a calibration

gas that was not procured from a QA approved vendor and no other QA controls were provided to assure the proper calibration

of the gas.On February 13, 1992, one containment

hydrogen monitor each in Units 1 and 3, were also determined

to have had surveillance

tests performed with calibration

gas that was not properly controlled

or calibrated.

This is a Severity Level IV violation (Supplement

1)applicable

to Units 1, 2 and 3.Page 2

ATTACHMENT

1 REPLY TO NOTICE OF VIOLATIONS

50-528/92-05-02, 50-528/92-05-0

t AND 50-528/92-05-03

NRC INSPECTION

CONDUCTED JANUARY 26, 1992-FEBRUARY 29, 1992 INSPECTION

REPORT NOS.50-528, 529, 530/92-05

0 REPLY TO NOTICE OF VIOLATION 50-528 92-05-02 Reason For The Violation The reason for both examples of the violation was a cognitive personnel error.During scheduled surveillance

testing of the Unit 1, number 1 steam generator low steam generator pressure trip setpoint on February 4, 1992, the RPS/ESFAS channel'B'ow steam generator pressure trips for both the number 1 and number 2 steam generators

were placed in bypass, as required by 36ST-9SB02,"PPS Bistable Trip Units Functional

Test." During this surveillance, the low steam generator pressure setpoint reset button was depressed, as required, resulting in the channel'B'ow steam generator pressure trip setpoint for both steam generators

being reduced to approximately

200 psia e below the actual steam generator pressures.

The surveillance

test subsequently

requires resetting of the channel'B'ow steam generator pressure trip setpoint to verify proper operation.

The channel'B'ow steam generator pressure trip setpoint for the number 1 steam generator was reset in accordance

with the surveillance

test procedure.

While checking the channel'B'ow steam generator pressure trip setpoint for the number 2 steam generator, the maintenance

I&C technician

performing

the surveillance

test did not select the number 2 steam generator low steam generator pressure setpoint on the select switch.This resulted in the maintenance

l&C technician

erroneously

using the previously

verified number 1 steam generator channel'B'ow steam generator pressure trip setpoint to check the numbers 2 steam generator channel'B'ow steam generator pressure trip setpoint.The RPS/ESFAS channel'8'ow steam generator Page 1 of 11

pressure trips for both the number 1 and number 2 steam generators

were taken out of bypass following completion

of the applicable

portion of the surveillance

test.N Approximately'one-half

hour after the channel'B'ow steam generator pressure trips were taken out of bypass, a Unit 1 control room reactor operator checked the low steam generator pressure trip setpoints as part of a scheduled setpoint check.The operations

procedure for control room data sheets (40DP-9OP05,"Control Room Data Sheet Instructions")requires any abnormal and/or unusual conditions

or readings be reported to the Shift Supervisor

or Assistant Shift Supervisor.

The control room reactor operator did not identify that the RPS/ESFAS channel'B'ow steam generator pressure trip setpoint for the number 2 steam generator was below the minimum allowed Technical Specification

value, as required.Corrective

Ste s That Have Been Taken And The Results Achieved Approximately

one hour after the control room reactor operator failed to identify the incorrect RPS/ESFAS channel'B'ow steam generator pressure trip setpoint for the Unit 1, number 2 steam generator, the Assistant Shift Supervisor

discovered

that the setpoint was below the minimum allowed Technical Specification

value.The channel'B'ow steam generator pressure trip for the number 2 steam generator was declared inoperable

and the Unit 1 maintenance

l&C department

was notified.The low steam generator pressure trip setpoint was reset to the required value approximately

one hour later.Page 2 of 11

A Condition Report/Disposition

Request was initiated to conduct an investigation

of this event and subsequently

determined

the cause to be personnel error.The involved control room reactor operator and maintenance

I8 C technician

have been disciplined

in accordance

with the APS Positive Discipline

Program.A control room night order discussing

this event was issued in Units 1, 2, and 3 to reinforce the importance

of attention to detail in performing

routine checks thoroughly.

Briefings have been conducted on this event with Units 1, 2, and 3 maintenance

l&C technicians.

As an enhancement, the surveillance

test procedure (36ST-9SB02)

has been revised to add detailed action steps to direct performers

on how to attain and determine the low steam generator pressure trip setpoints for added assurance that the minimum e allowed value for the trip setpoint is attained prior to removing the low steam generator pressure trip from bypass.The investigation

results were provided to the NRC in a letter from James M.Levine dated March 5, 1992 (Licensee Event Report 528/92-003-00).

Corrective

Ste s That Will Be Taken To Avoid Further Violations

The corrective

actions discussed above are considered

adequate to avoid further violations

and no additional

corrective

actions are planned.Page 3of11

~

Date When Full Com Ilance Will Be Achieved Full compliance

was achieved on February 4, 1992, upon restoring the Unit 1, steam generator number 2 low steam generator pressure trip setpoint.to

the minimum allowed Technical Specification

value.Additional

Information

The inspection

report cover letter requests an assessment

of the need for independent

verification

of the reactor trip setpoints adjusted during surveillance

testing.During the investigation

of this event, APS evaluated the need for independent

verification

of as-left reactor trip setpoints.

Although no previous examples of improper restoration

of reactor trip setpoints at the conclusion

of surveillance

testing were identified, APS e concluded that an additional

check of as-left reactor trip setpoints would be prudent, if the setpoint was.adjusted outside the acceptance

criteria during the surveillance

test.Surveillance

testing meeting this criteria was identified

for the low steam generator pressure trip and the low pressurizer

pressure trip.Changes to the PPS bistable trip units functional

test procedure (36ST-9SB02)

have been initiated to require a separate check to verify that the low steam generator pressure trip setpoint and the low pressurizer

pressure trip setpoint are within their acceptance

criteria prior to removing the trips from bypass.These changes will be implemented

by June 30, 1992.Page 4 of 11

REPLY TO NOTICE OF VIOLATION 50-528 92-05-01 Reason For The Violation The reason for the violation was an improper procedural

step and subsequent

implementation

of the flexibility

allowed by the step.Prior to February 25, 1992, during Unit 1 refueling activities, sixty incore instruments

,(ICIs)had been withdrawn in accordance

with maintenance

procedure 36MT-9RI06,"Withdrawal

Of The Incore Instruments

For Reactor Refueling Operations," leaving one ICI installed.

On February 25, 1992, scaffolding

had been erected at the entrance to the east end of the refueling canal.This scaffolding

prevented placement of the control element assembly (CEA)/ICI change platform above the ICI holding frame, and consequently

the use of the CEA hoist to withdraw the final ICI, as required by 36MT-9RI06, Step 8.4.5.The a involved Work Group Supervisor

reviewed 36MT-9RI06

for an alternate means to remove the final ICI.Step 7.7 of 36MT-9RI06

states,'This procedure should be considered

a guideline, the I&C technician

and Work Group Supervisor

should have flexibility

in the order of work performance

and should decide the need for some steps depending upon inspection

results, such as cleaning of slip tubes, spacers, etc.".The Work Group Supervisor

interpreted

this step as allowing a manual withdrawal

of an ICI, in lieu of using the CEA hoist, as required by 36MT-9RI06, Step 8.4.5.Following the decision to attempt a manual withdrawal

of the final ICI, a tailboard meeting was conducted, at which the ICI task shift lead was cautioned on the slow lift requirement

and the 500 pound maximum pull requirement

of 36MT-9RI06.

The radiationPage 5 of 11

0 protection

department

was notified of the planned ICI manual withdrawal.

.During the actual ICI withdrawal, a rope was attached to the ICI lift bail and used by a technician

on the 140 foot elevation platform to withdraw the ICI.A second technician, in the accompaniment

of a radiation protection

technician, was located in the refuel cavity to wipe the cable as it was withdrawn.

When the withdrawal

was first attempted, the force was greater than anticipated, so the technicians

stopped the withdrawal

attempt to investigate

the cause.A piece of duct tape was removed from the ICI cable and the ICI was successfully

withdrawn and secured in the ICI holding frame The duct tape had been left following a preceding, unrelated maintenance

activity to replace the ICI seal housing.Corrective

Ste s That Have Been Taken And The Results Achieved A Condition Report/Disposition

Request was initiated to investigate

this activity and determined

the cause discussed above.The B&W Nuclear Services personnel were briefed on the incident and the need for verbatim procedural

compliance

was emphasized.

Changes have been made to maintenance

procedure 36MT-BRI06,'Withdrawal

Of The Incore Instruments

For Reactor Refueling Operations," to delete the phrase,"this procedure should be considered

a guideline," from Step 7.7 (Step renumbered

as 2.1.2.7)and to revise Step 8.4,5 (Step renumbered

as 4.4.12)to allow lifting ICls manually.Page 6 of 11

0 Corrective

Ste s That Will Be Taken To Avoid Further Violations

The corrective

actions discussed above are considered

adequate to avoid further violations

and no additional

corrective

actions are planned.Date When Full Com Ilance Will Be Achieved Full compliance

was achieved on February 25, 1992, upon completion

of the manual withdrawal

of the final Unit 1 ICI.Page 7 of 11

REPLY TO NOTICE OF VIOLATION 50-528 92-05-03 Reason For The Violation The reason for the violation was inadequate

interim corrective

measures upon identification

of a quality deficiency.

A quality deficiency

report was initiated in April, 1991, to document that surveillance

test procedure 36ST-9HP03,"Containment

Hydrogen Monitoring

System Calibration

Test, Channel A," was inadequate

in that the test gas used was not traceable to a calibration

standard.An action plan was developed to address this deficiency

which included actions to establish technical specification

and quality requirements

for the test gas and locate an acceptable

vendor.The test gas used in this surveillance

was being purchased on a non-quality

related purchase order used to purchase miscellaneous

gases, without identifying

specific plant applications

for each gas.\Prior to an acceptable

vendor being approved, interim measures were taken to ensure the quality of the test gas used in the performance

of 36ST-9HP03.

A prospective

vendor (Air Products and Chemical)was selected based on their use by another Region V utility as a supplier of safety-related

calibration

gases.The prospective

vendor's quality assurance manual was reviewed and APS concluded that the vendor had adequate processes for ensuring that the required calibration

standards are accurately

represented

in their Certificates

of Analysis (CQA).APS also verified that the test gas being supplied by a local vendor was, in fact, being filled by Air Products and Chemical.Surveillance

test procedures, 36ST-9HP03

and 36ST-9HP04 (Containment

Hydrogen Monitoring

Page 8of11

System Calibration

Test, Channel B)were revised to require the serial number on the test gas bottle to be recorded during performance

of the hydrogen monitoring

system'urveillance

test to provide traceability

of the gas bottle.Following identification

of the critical design attributes

that are essential to the dedication

process of test gas, APS performed a commercial

grade survey of Air Products and Chemical and identified

some minor programmatic

issues, none of which would question the accuracy of the hydrogen concentration.

A randomly selected bottle of test gas filled by this vendor which had been supplied to APS was verified to contain the correct hydrogen concentration

during this survey.On January 9, 1992, due to an urgent need for hydrogen test gas, the system engineer and the Unit 1 l&C maintenance

department

authorized

a purchase of hydrogen e test gas filled by a local vendor using the existing non-quality

related purchase order.No test gas was in stock at APS and approximately

two weeks would have been necessary to obtain the test gas from Air Products and Chemical.Test gas was obtained from the local vendor and used in Unit 1.Although use of hydrogen test gas filled by the local vendor in a hydrogen monitoring

system surveillance

test was inappropriate, involved personnel did comply with interim corrective

measures.During the week of February 10, 1992, an NRC inspector was observing the hydrogen monitoring

system surveillance

test on a Unit 2 hydrogen analyzer and noted that the test gas being used was not traceable to the vendor being evaluated for acceptance

by APS.Based on this observation, all three units were checked for hydrogen test gas bottles which were not traceable to the vendor being evaluated for acceptance.

Three additional

test gas bottles were found, Page 9 of 11

which were not traceable to the vendor being evaluated for acceptance.

These bottles had been purchased under the non-quality

related purchase order for miscellaneous

gases and filled by a local vendor at various times.Corrective

Ste s That Have Been Taken and Results Achieved Hydrogen test gas bottles which were filled by the local vendor were removed from service, quarantined, and subsequently

returned to the vendor.Hydrogen monitoring

system surveillance

tests were performed on the hydrogen analyzers which had been tested using test gas bottles filled by the local vendor using test gas bottles filled by Air Products and Chemical.The tests required no adjustments

to hydrogen analyzers, thus validating

the tests performed using test gas bottles filled by H the local vendor.Air Products and Chemical has been accepted by APS as capable of providing test gases of the required'quality

and placed on the Commercial

Grade Approved Vendor's List.A quality related purchase order has been issued to Air Products and Chemical to establish a new stock level of test gases.The procurement/warehouse

tracking (class and item)numbers for test gas have been input into the Materials Management

Information

System and Station Information

Management

System for inclusion in corrective

maintenance

and surveillance

test work order packages associated

with'hydrogen

analyzers.

Page 10 of 11

r-

Corrective

S e s That Will Be Taken To Avoid Further Violations

The corrective

actions discussed above are considered

adequate to avoid further violations

and no additional

corrective

actions are planned.Date When Full Com liance Will Be Achieve Full compliance

was achieved on February 14, 1992, upon replacement

of the identified

test gas bottles which had been filled by the local vendor with test gas bottles filled by Air Products and Chemical.Page 11 of,11