ML042080435
| ML042080435 | |
| Person / Time | |
|---|---|
| Site: | Vermont Yankee File:NorthStar Vermont Yankee icon.png |
| Issue date: | 05/08/2003 |
| From: | Pichette A Entergy Nuclear Vermont Yankee |
| To: | Balduzzi M, Cosgrove B, Finn B, Jefferson S, Kilburn B, David Mannai, Mcelwee D, David Pelton, Porter B, Rondeau N, Sandstrum S, Beth Sienel, Skibniowski S, Wallin G, Wanczyk R, Robert Williams, Yialiades T - No Known Affiliation, Division Reactor Projects I |
| References | |
| FOIA/PA-2004-0267 | |
| Download: ML042080435 (8) | |
Text
. - ~Message- F~are. I 02 I Sienel, Beth From: Pichette, Ann Sent: Thursday, May 08, 2003 2:47 PM To: 'lerevents @inpo.org'; 'rbelval @velco.com'; 'gparker@ velco.com'; 'rivestE gmpvt.com';
'martin @gmpvt.com'; 'kvedar@ gmpvt.com'; 'dutton @gmpvt.com'; 'brown @gmpvt.com';
'william.sherman @state.vt.us'; 'bwendland@AmNuclns.com'; 'barbaralewis @platts.com';
'bamelan@cvps.com'; Kilburn, Bobbi; Balduzzi, Michael; Williams, Rob; Cosgrove, Brian; McElwee, David; Finn, Brian; Porter, Brad; Wanczyk, Robert; Yialiades, Theresa; Sandstrum, Sally; Jefferson, Stan; Mannai, David; Wallin, Greg; Rondeau, Nancy; Skibniowsky, Steve; Sienel, Beth; Pelton, David Attached please find the Vermont Yankee Nuclear Power Statlion Monthly Statistical Report for May 2003. If you have any questions please contact me.
Ann M. Pichette Controlled Document Specialist Technical Support Department (802)451-3094 6/15/2004
. MessageP Page~I of I Sienel, Beth From: Gill, Jeanne Sent: Thursday, April 10, 2003 1:50 PM To: 'lerevents @inpo.org'; 'rbelval @velco.com'; 'gparker@velco.com'; 'rivest @gmpvt.com';
'martin @gmpvt.com'; 'kvedar@ gmpvt.com'; 'dutton @gmpvt.com'; 'brown @gmpvt.com';
'william.sherman~state.vt.us'; 'bwendland @AmNuclns.com'; 'barbaralewis @platts.com';
'bamelan~cvps.com'; Kilburn, Bobbi; Balduzzi, Mike; Williams, Rob; Cosgrove, Brian; McElwee, David; Finn, Brian; Porter, Brad; Wanczyk, Robert; Yialiades, Theresa; Sandstrum, Sally; Jefferson, Stan; Mannai, David; Wallin, Greg; Rondeau, Nancy; Skibniowsky, Steve; Sienel, Beth; Pelton, David
Subject:
VERMONT YANKEE NUCLEQAR POWER STATION (ENTERGY NE) MSR MARCH 2003 Attached please find the Vermont Yankee Nuclear Power Station (Entergy NE) Monthly Statistical Report for March 2003.
Ifyou have any questions please contact me.
Jeanne A. Gill Technical Support Controlled Document Specialist 802451 3127 6/15/2004
Entergy Nuclear Northeast Entergy Nuclear Operations, Inc.
Vermont Yankee
-- n tergy 322 Governor Hunt Rd.
P.O. Box 157 Vernon, Vr C5354 Tel 802-257-7711 April 10, 2003 BVY-03-34 United States Nuclear Regulatoxy Commission ATTN: Document Control Desk Washington, D.C. 20555 I ,
Reference:
(a) License No. DPR-28 (Docket No. 50-271)
In'accordance with section 6.6.B of the Vermont Yankee Technical Specifications, submitted herewith is the Monthly Statistical Report for the Vermont Yankee Nuclear Power Station for the month of March, 2003.
Sincerey, Kevin H. Bronson General Manager, Plant Operations cc: USNRC Region I Administrator USNRC Resident Inspector USNRC Project Manager
VERMONT YANKEE NUCLEAR POWER STATION MONTHLY STATISTICAL REPORT 03-03 FOR THE MONTH OF MARCH 2003
OPERATING DATA REPORT DOCKET NO.50-271 DATE 030410 COMPLETED BY G.A. WALLIN TELEPHONE (802)258-5414 OPERATING STATUS
- 1. Unit Name: Vermont Yankee
- 2. Reporting Pericod: March
- 3. Licensed Thermal Power(MWt):1593
- 4. Nameplate Rating(Gross ryle): 540 I I
- 5. Design Electrical Rating(Net W~e): 522
- 6. Maximum Dependable Capacity(Gross Mite): 535
- 7. Maximum Dependable Capacity(Net MWe): 510
- 8. If changes, occur in capacity ratings(Items Number 3 through 7) since last report, give reasons:
- 9. Power level to which restricted, if any(Net NFWe): N/A
- 10. Reasons for restrictions, if any: N/A This Month Yr-to-Date Cumulative
- 11. Hours in Reporting Period 744.00 2160.00 265128.00
- 12. Number Of Hours Reactor was Critical 744.00 2160.00 225308.83
- 13. Reactor Reserve Shutdown Hours 0.00 0.00 0.00
- 14. Hours Generator On-Line 744.00 2160.00 221673.78
- 15. Unit Reserve Shutdown Hours 0.00 0.00 0.00
- 16. Gross Thermal Energy Generated(MWH) 1182174.40 3401416.75 335781833.54
- 17. Gross Electrical Energy Generated(MJH) 408799.00 1176377.00 112757307.00
- 18. Net Electrical Energy Generated(MTWH) 393094.00 1130743.00 107313102.00
- 19. Unit Service Factor 100.00 100.00 82.60
- 20. Unit Availability Factor 100.00 100.00 82.60
- 21. Unit Capacity Factor(Using MDC Net) 103.60 102.60 79.10
- 22. Unit Capacity Factor(Using DER Net) 101.20 100.30 77.50
- 23. Unit Forced Outage Rate 0.00 0.00 3.90
- 24. Shutdowns scheduled over next 6 months(Type, Date, and Duration of Each: N/A
- 25. If shut down at end of report period, estimated date of startup: N/A
- 26. Units In Test Status(prior to commercial operation): N/A Forecast Achieved INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION VYDPF 0411.01 (Sample)
DP 0411 Rev. 8 Page 1 of 1 RT No. 13.F01.19F
AVERAGE DAILY UNIT POWIER LEVEL DOCKET NO. 50-271 UNIT Vermont Yankee DATE 030410 COMPLETED BY G.A. WALLIN TELEPHONE (802)258-5414 MONTH March DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MLve-Net) (X.We-Net)
- 1. 530 17. 529
- 2. 530 18. 530
- 3. 530 19. 529
- 4. 530 20. 529 D. 530 21. 529
- 6. 529 22. 529
- 7. 530 23. 530
- 8. 530 24. 529
- 9. 530 25. 529
- 10. 529 26. 529
- 11. 529 27. 529
- 12. 529 28. 529
- 13. 529 29. 529
- 14. 529 30. 495
- 15. 530 31. 529
- 16. 529 INSTRUCTIONS:
On this format, list the average daily unit power level in MWE-Net for each day in the reporting month. Compute to the nearest whole megawatt.
VYDPF 0411.02 (Sample)
DP 0411 Rev. 8 Page 1 of 1 RT No. 13.FO1.18V
UNIT SHUTDOWNS AND POWER REDUCTIONS REPORT MONTH M4ARCII DOCKET NO 50-271 UNIT NAME Vermont Yankee DATE 030410 COMPLETED BY G.A. Wallin TELEPHONE (802)258-5414 12 3 45 No. Date Type Duration Reason Method of License System Component Cause and Corrective (hours) Shutting Event Code Code Action to Prevent DoRat Report ff Recurrence
_______ ~Reactor__ _ _ _ _ _ _ _ _ _ _ _ _ _ _
03-03 030329 F 0.00 A 4 N/A PIC CKTBRK Relay failure on 379 ATB Power causing logic trip to open Reduction 381, 379, 79-40 ATB's and K-i OCB.
1 F: Forced 2 Reason: 3 Method: 4 Exhibit G- Instructions S: Scheduled A-Equipment Failure (Explain) 1 - Manual for Preparation of Data B-Maintenance or Test 2 - Manual Scram Entry Sheets for License C-Refueling 3 - Automatic Scram Event Report (LER) File D-Regulatory Restriction 4 - Other (Explain) (NUREG 0161)
E-Operator Training and.
License Examination 5 Exhibit I - Same Source VYDPF 0411.03 F-Administrative DP 0411 Rev. 8 G-Operational Error (Explain)
Page 1 of 1 II-(Explain)
.... . I .. .
DOCKET NO. 50-271 DATE 030410 COMPLETED BY G.A. WALLIN TELEPHONE (802)258-5414
- REPORT MONTH March SUMQ4RY OF OPERATING EXPERIENCES Highlights Vermont Yankee operated at 99.7 of rated thermal power for the month.
Gross electrical generation was 408,799 MWHe or 100.6% design electrical capacity.
Operating Summary The following is a chronological description of plant operations including other pertinent items of interest for the month:
At the beginning of the reporting period the plant was operating at 99.9%
of rated thermal power.
030329 At 2143 hours0.0248 days <br />0.595 hours <br />0.00354 weeks <br />8.154115e-4 months <br />, a relay failed on the 379 Air Trip Breaker causing logic to trip open 381, 379, 79-40 ATB's and the K-1 Oil Circuit Breaker. (See Unit Shutdowns and Power Reductions) 030330 At 0005 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />, commenced power reduction to 77%.
030330 At 0519 hours0.00601 days <br />0.144 hours <br />8.581349e-4 weeks <br />1.974795e-4 months <br />, following isolation of 379 ATB and breakers 381, 79-40, and K-1 being closed; a return to full power was initiated.
At the end of the reporting period the plant was operating at 99.9% of rated thermal power.
VYDPF 0411.04 (Sample)
DP 0411 Rev. 8 Page 1 of 1 RT No. 13.FO1.18X