ML20071H462
| ML20071H462 | |
| Person / Time | |
|---|---|
| Site: | Pilgrim |
| Issue date: | 06/30/1994 |
| From: | Munro W, Olivier L BOSTON EDISON CO. |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| 94-078, 94-78, NUDOCS 9407150177 | |
| Download: ML20071H462 (7) | |
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Tech. Spec. 6.9.A.2 G
Boston Edison Pilgon Nuclear Power Station Rocky Hdt Road Plymouth, Massachusetts 02360 L. J. Olivier Vice President Nuclear Operations Julv 14 , 1994 and station Director BECo atr. #94- 078 l
U.S. Nuclear Regulatory Commission Attention: Document Control Desk Washington, DC 20555 Docket No. 50-293 License No. DPR-35 JUNE 1994 MONTHLY REPORT In accordance with PNPS Technical Specification 6.9.A.2, a copy of the Operational Status Summary for Pilgrim Nuclear Power Station is attached for your information and planning. Should you have any questions concerning this report please contact me directly.
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y J. Olivier WJM/ lam /9458 Attachment cc: Mr. Thomas T. Martin Regional Administrator, Region I U.S. Nuclear Regulatory Commission 475 Allendale Road King of Prussia, PA 19406 Senior Resident Inspector 9407150177 940630 p i PDR ADOCK 05000293 ,
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. OPERATING DATA REPORT DOCKET NO. 50-293 l DATE July 14, 1994 ;
COMPLETED BY: W. Munro i TELEPHONE (508) 830-8474
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OPERATING STATUS NOTES
- 1. Unit Name Pilgrim I
- 2. Reporting Period May 1994
- 3. Licensed Thermal Power (MWt) 1998
- 4. Nameplate Rating (Gross MWe) 12H
- 5. Design Electrical Rating (Net MWe) HEE
- 6. Maximum Dependable Capacity (Gross MWe) HRH
- 7. Maximum Dependable Capacity (Net MWe) 510
- 8. If Changes Occur in Capacity Ratings (Item Number 3 Through 7) Since Last Report, Give Reasons:
NONE
- 9. Power Level To Which Restricted, If Any (Net MWe): None
- 10. Reasons For Restrictions, If Any: N/A This Month Yr-to-Date Cumulative
- 11. Hours in Reporting Period 720._Q 4343.0 118975.0
- 12. Hours Reactor Critical 720.0 4050.0 116991.5
- 13. Hours Reactor Reserve Shutdown 0.0 Q1H 0.0
- 14. Hours Generator On-Line 720.0 3930.8 112719.8
- 15. Hours Unit Reserve Shutdown Em0 0.0 2Q
- 16. Gross Thermal Energy Generated MWH) 1419936.0 7453368.0 198606312.0
- 17. Gross Electrical Energy Generated (MWH)487010.0 2556260.0 67202194.H .
- 18. Net Electrical Energy Generated (MWH) 468820.0 2460133.0 64593827.0
- 19. Unit Service Factor 100.0 90.5 59.,6
- 20. Unit Availability Factor 100.0 90,5 59.6
- 21. Unit Capacity Factor (Using MDC Net) 97.2 84,5 51.0
- 22. Unit Capacity Factor (Using DER Net) 99.4 86.5 52.2 ;
- 23. Unit Forced Outage Rate R20 4.6 11,6
- 24. Shutdowns scheduled over next 6 months (type, date, and duration of each) - MCO-10 October (30 Days)
- 25. If shutdown at end of report period, estimated date of startup - UNIT OPERATING .
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AVERAGE DAILY UNIT POWER LEVEL I l
DOCKET NO. 50-293 '
DATE: July 14, 1994 f
COMPLETED BY: W. Munro TELEPHONE: (508) 830-8474 MONTH June 1994 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) (MWe-Net) 1 661 17 659 2 660 18 661 3 660 19 525 4 658 20 660 5 659 21 660 6 660 22 661 7 662 23 660 8 660 24 658 9 660 25 659 10 558 26 660 11 659 27 630 12 660 28 662 13 660 29 661 14 662 30 661 15 661 16 659 i
I This format lists the average daily unit power level in MWe-Net for each l day in the reporting month, computed to the nearest whole megawatt. l 1
BOSTON EDISON COMPANY PILGRIM NUCLEAR POWER STATION DOCKET NO. 50-293 OPERATIONAL
SUMMARY
FOR JUNE 1994 The unit started the reporting period at approximately 100 percent core thermal power (CTP). This power level was essentially maintained until ;
June 10, 1994. At 1054 hours0.0122 days <br />0.293 hours <br />0.00174 weeks <br />4.01047e-4 months <br /> cr June 10, 1994, the "A" Recirculation Pump 1 Motor Generator (MG) Set tripped, and power was reduced to approximately 41 percent CTP at 1141 hours0.0132 days <br />0.317 hours <br />0.00189 weeks <br />4.341505e-4 months <br />. At 1432 hours0.0166 days <br />0.398 hours <br />0.00237 weeks <br />5.44876e-4 months <br />, following troubleshooting, the "A" Recirculation Pump MG Set was restarted and reactor power was increased. AT 1914 hours0.0222 days <br />0.532 hours <br />0.00316 weeks <br />7.28277e-4 months <br />, 100 percent power was attained, and was essentially maintained until June 19, 1994, when power was reduced to j approximately 47 percent CTP to facilitate a planned thermal backwash of the main condenser. Following completion of the backwash, power was increased to 100 percent CTP at approximately 1530 hours0.0177 days <br />0.425 hours <br />0.00253 weeks <br />5.82165e-4 months <br /> where it was essentially maintained until June 27, 1994. At 0400 hours0.00463 days <br />0.111 hours <br />6.613757e-4 weeks <br />1.522e-4 months <br /> on June 27, 1994, power was reduced to approximately 73 percent CTP due to a malfunction of the "A" 3rd Point Feedwater Heater Level Control]er.
Following maintenance to restore the feedwater heater to service, power was increased, reaching 100 percent CTP at approximately 0800 hours0.00926 days <br />0.222 hours <br />0.00132 weeks <br />3.044e-4 months <br />, where it was maintained for the remainder of the reporting period.
SAFETY RELIEF VALVE CHALLENGES MONTH OF JUNE 1994 Requirement: NUREG-0737 T.A.P. II.K.3.3 l
There were no safety relief valve challenges during the reporting period.
An SRV challenge is defined as anytime an SRV has received a signal to '
operate via reactor pressure, auto signal (ADS) or control switch (manual).
Reference BECo Ltr. #81-01 dated January 5, 1981.
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REFUELING INFORMATION The following refueling information is included in the Monthly Report as requested in an NRC letter to BECo, dated January 18, 1978:
For your convenience, the information supplied has been enumerated so that each number corresponds to equivalent notation utilized in the request.
- 1. The name of this facility is Pilgrim Nuclear Power Station, Docket !
Number 50-293.
- 2. Scheduled date for next refueling shutdown: April 1, 1995.
- 3. Scheduled date for restart following next refueling: May 26, 1995.
- 4. Due to their similarity, requests 4, 5, & 6 are responded to collectively under #6.
- 5. See #6.
- 6. The new fuel lc Jied during the 1993 refueling outage was of the same design as loaded in the previous refueling outage and consisted of 140 assemblies.
- 7. (a) There are 580 fuel assemblies in the core.
- 03) There are 1629 fuel assemblies in the spent fuel pool.
- 8. (a) The station is presently licensed to store 3859 spent fuel assemblies. The actual usable spent fuel storage capacity is 2320 fuel assemblies.
- 03) The planned spent fuel storage capacity is 3859 fuel assemblies.
- 9. With present spent fuel in storage, the spent fuel pool now has the capacity to accommodate an additional 691 fuel assemblies.
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MONTH JUNE 1994 . .
f PILGRIM N'JCLEAR POWER STATION MAJOR SAFETY RELATED MAINTENANCE -
CORRECTIVE ACTION TO ASSOC SYSTEM COMPONENT MALFUNCTION CAUSE MAINTENANCE PREVENT RECURRENCE LER Salt Service SSW Pump Degraded Age related Replaced P-208A None N/A Water (SSW) P-208A Motor performance degradation motor with new ,
System motor of improved design. (Mfr.
Balanced motor and pump per Procedure 3.M.1-15 r -
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-y UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO: 50-293 DOCKET NO: 50-293 '.
NAME: Pilgrim I DATE: July 14, 1994 COMPLETED BY: W. Munro TELEPHONE: (508) 830-8474 REPORT MONTH: June 1994 l METHOD OF LICENSE SYSTEM COMPONENT CAUSE & CORRECTIVE TYPE DURATION REASON SHUTTING DOWN EVENT CODE CODE ACTION TO PREVENT NO. DATE 1 (HOURS) 2 REACTOR REPORT 4 5 RECURRENCE
- 7 6/19/94 S 0.0 B N/A N/A N/A N/A Power reduction to facilitate a thermal i backwash of the main condenser i
1 2 3 4&5 F-Forced A-Equip Failure 1-Manual Exhibit F&H ;
S-Sched B-Main or Test 2-Manual Scram Instructions for l C-Refueling 3-Auto Scram Preparations of ;
D-Regulatory Restriction 4-Continued Data Entry Sheet i E-Operator Training 5-Reduced Load Licensee Event Report l
& License Examination 9-Other (LER) File (NUREG-1022)
F-Admin :
G-Operator Error H-Other o
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