ML20127H405
| ML20127H405 | |
| Person / Time | |
|---|---|
| Site: | Quad Cities |
| Issue date: | 06/12/1985 |
| From: | Chrissotimos N NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
| To: | |
| Shared Package | |
| ML20127H345 | List: |
| References | |
| TASK-1.A.2.1, TASK-2.B.4, TASK-2.K.3.16, TASK-2.K.3.21, TASK-2.K.3.24, TASK-2.K.3.35, TASK-TM 50-254-85-12, 50-265-85-13, NUDOCS 8506260323 | |
| Download: ML20127H405 (15) | |
See also: IR 05000401/2005031
Text
_ _
.
.
U. S. NUCLEAR REGULATORY COMMISSION
REGION III
Reports No. 50-254/85012(DRP); 50-265/85013(DRP)
Docket Nos. 50-254; 50-265 Licenses No. OPR-29; DPR-30
Licensee: Commonwealth Edison Company
Post Office Box 767
Chicago, IL 60690
Facility Namc: Quad Cities Nuclear Power Station, Units 1 and 2
Inspection At: Quad Cities Site, Cordova, IL
Inspection Conducted: April 1 through May 31, 1985
Inspectors: A. L. Madison
A. D. Morrpngfello_
Approved By: is 41ii5s, M d f- B T
Reactor Projects Section 2C Date /
Inspection Summary:
Inspection on April 1 through May 31, 1985 (Reports No. 50-254/85012(DRP);
50-265/85013(DR))
Areas Inspected: Routine, unannoun'ced inspection by the resident inspectors
of actions on previous inspections findings; operations; radiological controls;
maintenance / modifications; surveillance; housekeeping; procedures; fire
protection; emergency preparedness; security; quality assurance; quality
control; administration; routine reports; LER review; TMI items; regional
requests; Headquarters requests; and independent inspection. The inspection
involved a total of 542 inspector-hours onsite by two MRC inspectors,
including 50 inspector-hours onsite during offshifts. .
Results: No violations or deviations were identified. Minor areas of concern
were identified in operations surveillance, Quality Assurance, and procedures.
Overall, the licensee's performance has remained steady.
O
.
k
.
4
.
DETAILS
. 1. Persons Contacted
- N. Kalivianakis, Superintendent
D. Bax, Assistant Superintendent for Maintenance
T. Lihou, Technical Staff Supervisor
R. Roby, Senior Operating Engineer
- N. Griser, Senior Quality Assurance Specialist
The inspectors also interviewed several other licensee employees,
including shift engineers and foremen, reactor operators, technical
staff personnel, and quality control personnel.
- Denotes those present at the exit interview on May 31, 1985.
2. Routine Inspection
The resident inspectors, through direct observation, discussions with
licensee personnel, and review of applicable records and logs, examined
the areas stated in the inspection summary and accomplished the following
inspection modules:
37701 Facility Modifications
42700 Plant Procedures
61701 Surveillance
61726 Monthly maintenance observations
62703 Monthly maintenance observations
71707 Operational safety verification
71710 ESF system walkdown
71711 Review of plant operations
90713 Review of periodic and special
reports
92700 Onsite review of LERs
l 92701 TMI Action Items
92702 Onsite followup of Events
92703 IE Bulletin followup
92704 Headquarters Requests
92705 Regional requests
92706 Independent inspection
93702 Onsite followup of events
The inspectors verified that activities were accomplished in a timely
manner using approved procedures and drawings and were inspected / reviewed
as applicable; procedures, procedure revisions and routine reports were
in accordance with Technical Specifications, regulatory guides, and
industry codes or standards; approvals were obtained prior to initiating
any work; activities were accomplished by qualified personnel; the
Ifmiting conditions for operation were met during normal operation and
while components or systems were removed from service; functional testing
and/or calibrations were performed prior to returning :omponents or
2
.
.
.
systems to service; independent verification of equipment lineup and
-
. review of test results were accomplished; quality control records and
logs were properly maintained and reviewed; parts, materials, and
equipment were properly certified, calibrated, stored, and or maintained
as applicable; and adverse plant conditions including equipment
malfunctions, potential fire hazards, radiological hazards,. fluid leaks,
excessive vibrations, and personnel errors were addressed in a timely
manner with sufficient and proper corrective actions and reviewed by
appropriate management personnel.
Further, additional observations were made in the following areas:
a. Action on Previous Inspection Findings
(Closed) Open Item 254/84-14-01 Improper Installation of Steam
. Jet. Air Ejector Valves. This item was addressed in IE Report
No. 254/85-02 and dispositioned as an example of an item of
noncompliance. As such, no further actions are required.on
this Open Item.
(Closed) Open Item 254/84-23-02 and 265/84-21-01 Revise QGP 2-4
" Shutdown From Power Operations To Hot Standby" and QOP 207-2'
" Declaring Rod Worth Minimizer Computer Inoperable." These
changes were required due to difficulties experienced on
October 25, 1984~and the scram that resulted on Unit 2. QGP 2-4
was revised to allow hot shutdown to include having the Main Steam
-Isolation Valves open and thus facilitate pressure control.
.QOP 207-2 was revised to eliminate the confusion experienced
by operators'on October 25, 1985. Both revisions were reviewed
by the resident inspectors and found to be acceptable. No further
actions are required.
(Closed) Open Item 265/84-10-01 JumperMo'dificationToStandby
Gas. Treatment System Heaters.. This item was= addressed.in IE
Report 265/85-02 and dispositioned as-an example of an item of
noncompliance. 'As such, no further actions are required on this
Open Item.
(Closed) Unresolved Item 254/85004-01 and 265/85004-02 High Pressure
Coolant Injection (HPCI) Room Coolers.
This item tracked resolution of the concern for HPCI room cooler fan
environmental qualification requirements. The room coolers must be
operable to ensure' operability and thus the concern. However, it
was determined that the postulated line break that would cause a
harsh environment for the fans is a HPCI line break. Therefore,
HPCI would be inoperable and there would be no need for the room
coolers. Since the normal environment for the fan is mild, this
equipment need not be environmentally qualified.
No violations or deviations were identified.
.
3
,
.
.. . . - . . .-. - - - . ._, _ _ . -- ..
l
$ l
+
1- -
b. Plant Operation
Unit 1 was in operation and Unit' 2 was shutdown for refueling at
the beginning of the report period. On May.7, 1985 two contractor
, employees were injured when an electrical cable they were using
came into contact with the Unit 2 345 Kilovolt power line, which
1- was providing offsite power to Unit 2. The Unit 2 auxiliary
transformer tripped, causing a loss of offsite power to Unit 2
. and a voltage transient on Unit 1. The voltage transient on Unit 1
caused the isolation of several feedwater heaters and a loss of air
to the feedwater~. regulating valve. The Unit 1 operator responded
to the loss of feedwater heaters by reducing recirculation flow,
_ thus. reducing power. However, the loss of air to the feedwater
. regulating valve prevented its automatic response and the reactor F
Lutomatically scrammed when reactor water level reached the scram
setpoint. ~During the event, the Emergency Notification System (ENS)
phones lost power. Recent changes due to the breakup of the AT & T ,
- and also due to system upgrades (replacing old wires with fiber
4
optics) have placed ENS in a configuration not in conformance with
p the licensee's response to IE Bulletin 80-15. The licensee agreed
to revise this response.
'
'
At present the ENS phones receive power from the Instrumentation
Bus -:a very reliable source. However, as recent events point out,
-
this power source can be lost. Therefore, a single source of power
'
for this system is unsatisfactory. The licensee has committed.to
installing a new phone system which'will have a backup battery
supply. This backup battery will also supply the ENS phones.
Completion of these modifications will be tracked as an open' item
,
l Power was restored to Unit 2 by the 1/2 emergency diesel generator
and by a cross-tie to the Unit 1 auxiliary transformer. Repairs to
~
i the transformer were completed May 8, 1985, and normal power was
restored to Unit 2.
- Unit I remained shutdown to facilitate replacement of the station
i 125 volt batteries and modifications to the 1/2 emergency diesel
generator to comply with Appendix R commitments. Unit 1 returned
to power on May 17, 1985.
On May 22, 1985, while. performing the monthly operability test, the
1/2 diesel generator was declared inoperable due to a problem in the
-
diesel ~ generator cooling water pump circuitry. A modification had
been performed on the 1/2 diesel generator to allow for switching
between power sources for the cooling water pump as part of
. Appendix R commitments. Panels were obtained from the Hatch Co.
of El Paso, Texas. 'These panels contained thermal overloads and a
fuse as an integral part of the circuitry. The problem with this
circuitry was that neither the fuse nor the thermal overloads were
annunciated in the control room. When these protective devices
operated, the control room did not know that the cooling water pump
had tripped.
4
n l
.
.
Later that day, while performing Core Spray logic tests, the Unit 2
diesel generator started as required but tripped'due to loss of
control power. An Unusual Event was declared. The 1/2 diesel
generator was tested and declared operable thus terminating the
Unusual Event. The Senior Resident Inspector questioned the
operability of the 1/2 diesel generator and the ifcensee responded
by jumpering out the thermal overload device and'the fuse.
The Hatch Co. panels containing thermal overloads was considered a
potentially generic item of concern and was forwarded to Region III
for action.
At 1800 on May 30, 1985 Unit 1 experienced a scram from approximately
100% power. A shift foreman was placing the Turbine Steam Chest
pressure instrument back in service which caused vibration on the
instrument rack. This rack also contained main steam line low
pressure instrumentation which, when shocked, caused a Group I
isolation and the Main Steam Isolation valve closure resulted in
a scram. During scram recovery, the unit experienced a second
scram. This came from low vessel level when the MSIV's were
reopened to reduce reactor pressure. No ECCS systems were called
upon and all systems operated as expected.
Both units were shutdown at the close of this report perioc'.
During plant tours of Units 1 and 2, the inspectors walked down the
. accessible portions of the Core Spray Systems and the Residual Heat
Removal Systems and performed the applicable portions of Inspection
Procedure 71710 "ESF System Walkdown."
'
No-violations or deviations were identified.
'
c. Maintenance
The following activities were observed / reviewed:
(1) Observed installation of Electrical Switchgear for Appendix R
modifications on Unit 2 emergency diesel generator.
(2) Observed and reviewed overhaul of Unit 2 High Pressure Coolant
Injection system turbine.
(3) Observed preparations for weld overlays on recirculation system
piping for Unic 2.
(4) Observed and reviewed installation and testing of Unit 2 Scrci-
Discharge Volume.
(5) Observed Mechanical Maintenance installing Temperature Control
Valve on RBCCW.
.
5
.
.
(6) Observed Instrument Maintenance installing new control for
(7) Observed Mechanical Maintenance repairing discharge valve of
Unit 2 CRD pump.
(8) Observed Instrument Mechanical repairing LLRT gauge (replacement
of diaphragm in pressure regulator).
(9) Observed Mechanical Maintenance and factory representatives
working on new Target Rock safety relief valve.
(10) Observed Mechanical Maintenance repairing TBCCW pump and
installation of same.
(11) Observed Electrical Maintenance installing new battery racks
for Unit 2 125 VDC.
(12) Observed in house leak rate test of one Electromatic Relief
Valve.
(13) Observed Mechanical Maintenance and factory representative
inspecting Unit 2 diesel generator.
During Local Leak Rate Testing (LLRT) of the Main Steam Isolation
Valves (MSIV) the 28 and 2D outboard MSIV's showed leakage in excess
of the allowable leakage. The resident inspector observed the MSIV
seats and disc after disassembly and they appeared to be free of any.
foreign matter and no cracks were visible on the surfaces. The 28
MSIV repairs consisted of lapping the main seat and disc and the
pilot valve seat and disc. This MSIV was retested and failed. The
process was repeated and the valve still failed. The main disc was
replaced and the valve passed the LLRT.
The 2D MSIV repairs consisted of lapping the main seat, pilot seat
and disc and replacement of the main disc. The valve was reassembled
and successfully tested.
d. Surveillance
The following activities were observed / reviewed:
(1) Reviewed Reactor Vessel Low Low Water level functional test
Unit 2 and Unit 1
(2) Reviewed testing of newly installed analog trip system, Unit 2.
(3) Reviewed high drywell pressure functional test for Unit 2. l
(4) Observed preparations for and recovery from integrated leak l
'
rate testing for Unit 2.
l
6
. . . - . - . - - - -- . , .- -
.
.
(5) Observed Local Power Range Monitor calibrations on Unit 2.
(6) Observed one channel of Core Spray Logic testing on Unit 2.
(7) Observed rod scram timing on Unit 2.
(8) Observed 25% of RHR logic test on Unit 2.
(9) Observed 50% of Auto Start SBGTS tests on Unit 2.
(10) Observed Electrical Maintenance performing surveillance on
various EQ breakers.
On May 17, 1985, Unit 2 experienced a Group II isolation signal due
to surveillance activities. While 2A drywell radiation monitor was
inoperable for repair purposes, surveillance of the newly installed
analog trip system was performed. Again, on May 18, 1985 with the
2A drywell radiation monitor still inoperable for repair purposes,
surveillance was performed on high Drywell Pressure instrumentation
causing another Group II isolation. These unnecessary challenges of
plant safety systems could have been avoided with proper communication
and planning by the operations department. Operations personnel, by
being fully aware of plant and equipment status should be able to
foresee the results of surveillance testing and take actions to
prevent unnecessary safety system actuations. The inspectors
communicated this concern to licensee plant management and will
continue to observe this area for improvement.
e. Procedures Reviewed
The following procedures were reviewed:
QAP 200-13, Revision 10 Station Housekeeping Organization
,0AP 200-S2, Revision 1 Individual Housekeeping Surveillance
QAP 200-S3, Revision 1 Fire Protection and Housekeeping
Discrepancies
QAP 200-S4, Revision 1 Periodic Fire Inspection Report
QAP 200-S5, Revision 1 Housekeeping Inspection Report
QAP 200-S6, Revision 1 Housekeeping Inspection
QAP 200-T3, Revision 1 Housekeeping Zone Descriptions and
Designations
QAP 900-4, Revision 1 Traceability Tag Procedure
QAP 1900-3, Revision 15 Station Access Control
7
__
.
. . ,
'QAP 1900-T9, Revision :1
'
Possession of a Firearm Within the'
Station Protected Area
QMP 800-21, Revision 1- Disassembly, Repair, and Reas'sembly of
Safety-Related Butterfly, Ball, and
Check Valves with Pneumatic or
' Hydraulic Actuators
QMP 800-S16, Revision 1- Safety-Related Butterfly, Ball, or
Check Valve and Actuator Checklist
QMP 800-T22, Revision 1 ' Butterfly, Ball and Check Valve Shaft
Scribe Orientation
QMP 100-S11', Revision 2 Request for'Limitorque Valve Torque
Switch Setpoint Change
QAP 900-5,. Revision 1 In-Plant Radiography--Required
Notifications and. Actions
'
QAP 1900-10, Revision 10 Security Identification Badge / Key-Card
Assignment and Control
QFP 100-1, . Revision 11. Master Refueling Procedures
QFT 100-4, Revision 4 Refueling Interlock Check (Checklist
Included)
QMP 800-22, Revision 2 Target Rock Safety / Relief Valve Removal
and Installation
QMS 100-1, Revision 6 Monthly Fire Inspection
QMS'100-52, Revision 8 Unit 1 and Unit 2 "R" Area Monthly Fire
Inspection Check Sheet
f. Quality Assurance.
During a Quality Assurance (QA) audit in October, 1984,-it was
determined by the Licensee that the vendor of electrical switchgear,
Hatch Inc. of El Paso, Texas, had not submitted approved welding-
procedures and other documentation to assure quality. In April,
1985, acceptable' documentation was submitted. However,.a review-
by the on-site Q.A. manager identi'fied that while the' documentation
was for Shielded Metal Arc Welding (SMAW) the cabinets had actually
'been welded using Gas Metal Arc Welding (GMAW). Further-
investigation at the vendor's facility determined that Hatch, Inc.,
management personnel were unaware of the actual procedures >being .
used for arc welding in their shop.
~
8
.
.
.
The licensee then reviewed the vendor's procedures for GMAW and
~
contacted the four welders involved in cabinets supplied to Quad
Cities to certify them to GMAW standards. This involved
considerable effort in that two of the welders no longer worked
for Hatch. All four welders passed certification testing and
the procedures were found acceptable.
A sample of the cabinets had been " Shaker" tested by Wyle Labs and
found adequate for Seismic qualifications. All other cabinets at
Quad Cities Station were compared to these samples by drawing weld
maps and comparing weld dimensions. Further, vendor Quality Control
(QC) inspections were reviewed for adequacy (the QC inspector had
performed 100% inspection) and the QC inspector was interviewed by
the licensee to verify his qualifications.
Region III dispatched a specialist to review the licensee's
,
actions and inspect the cabinet welds. The welds were found
adequate and the cabinets were released for use at the station.
'
These particular cabinets were being installed as safety-related
and were required to meet seismic qualifications as part of
10 CFR 50 Appendix R upgrade modifications being made to the
The second problem is one of communications. These cabinets s,hould
have been placed on hold pending resolution of QA concerns. However,
due to lack of adequate communication, the personnel who performed
the receipt inspections for these cabinets were unaware of these
concerns. Thus the cabinets were accepted and installed.
Fortuitously, none of the cabinets were ever put into operation.
Formal mechanisms are in place to ensure proper communication of QA
concerns. Therefore, no specific corrective actions are required by
-
the ifcensee. However, the licensee was cautioned by the resident
inspectors and agreed that better communication must be maintained
in the future.
No violations or deviations were identified.
g. Review of Review of Routine and Special Report
The inspectors reviewed the monthly performance report for Units 1
and 2 for the months of March and April, 1985.
No violations or deviations were identified.
h. LER Review
(1) (open) LER 85005, Revision 0 and Revision 1: Unit 1
Fuel Pool Monitor Trips.
.
9
.
L-
-.
c
.
This report documents several spurious. trips of the 1A fuel
pool monitor caused by electronic noise. Difficulty in
isolating the cause of the noise accounted for the number
of spurious trips. Troubleshooting by the Instrument.
Maintenance department continues - as yet no specific cause
has been found. This LER will remain open pending satisfactory
repair of the monitor. ,
(2)- (open) LER 85012, Revision 0, Unit 1: 1A Fuel Pool Monitor
Trip.-
Refer to above LER
(3) (open) LER 85014, Revision 0, Unit 1: 1A Fuel Pool monitor
. Trip (refer to LER 85005).
(4) (closed) LER 85002, Revision 0, Unit 2: High Pressure Ccolant
Injection Inoperable.
On January 29, 1985, Unit 2 was operating at 100 percent
thermal power. At 2300 hours0.0266 days <br />0.639 hours <br />0.0038 weeks <br />8.7515e-4 months <br /> it was discovered that the
High Pressure Coolant Injection (HPCI) System's Motor Gear
Unit.(MGU) failed to stay at its High Speed Stop. HPCI was
declared inoperable and the required Technical Specifications
surveillances were initiated. A jumper was placed on the
HPCI's MGU.* HPCI was then declared operable and HPCI
operability tests were performed. During these operability
tests, HPCI injection valve, M0 2-2301-8,.would not open when .
it was given an OPEN signal from the Control Room. HPCI was
declared inoperable again. At 0300 hours0.00347 days <br />0.0833 hours <br />4.960317e-4 weeks <br />1.1415e-4 months <br /> a Generating Station
. Emergency Procedure (GSEP) Unusual Event was declared when the.
decision was made to shutdown.
The cause of the MGU failure was traced to a failed capacitor.
The cause of the valve failure was found to be a broken torque
switch. The problems were repaired and the GESEP Unusual Event-
was terminated at 1530 hours0.0177 days <br />0.425 hours <br />0.00253 weeks <br />5.82165e-4 months <br /> on January 30, 1985. No further
actions are required.
(5) (open) LER 85006, Revision-0, Unit 2: Main Steam Isolation
Valves (MSIV's) fail Local Leak Rate Tests (LLRT).
This report documents the failure of MSIV's A0-2-203-2B and D
to pass LLRT. -When the causes for failure have been determined-
and repairs have been completed, a supplemental report will be
issued. This LER will remain open pending receipt of that
supplemental. report.
(6) (open) LER 85008, Revision 0, Unit 2: Linear Indications on
. Reactor. Rec'irculation System Welds.
!
i
10
.
-a-_ . . _ _ _ __ _ _ _. _ _ _ _ _ _ _ . _ _ _ . - _ . - . _ _ _ _ .______.__a--r*+
.
?
This report documents the finding of crack indications during
normal In-Service Inspection (ISI). The cause is postulated
as being intergranular stress corrosion cracking. Further
analysis were performed and repairs (weld overlay) were
accomplished. A supplemental report will be issued after all
reviews are completed. This LER will remain open pending
receipt of that supplemental report.
(7) (closed) LER 85009, Revision 0, Unit 2: 2A Fuel Pool Radiation
Monitor Trip.
On March 20, 1985, Unit Two was shutdown for the End of Cycle
Seven Refueling and Maintenance Outage. At 0230 hours0.00266 days <br />0.0639 hours <br />3.80291e-4 weeks <br />8.7515e-5 months <br />, the 2A
Fuel Pool Radiation Monitor spiked above its trip setpoint
of 100 mr/ hour, isolating the Reactor Building Ventilation
starting the Standby Gas Treatment System. The 2A Fuel
Pool Radiation Monitor tripped because of the transfer of the
Steam Dryer from the Reactor cavity to the Dryer-Separator
storage pit. Radiation levels in the area around the Reactor
cavity were monitored continuously and were not excessive.
Since the Reactor Building Ventilation System and the Standby
Gas Treatment System performed as designed, the safety
consequences nf this occurrence were minimal.
The cause of this occurrence was procedural inadequacy.
Maintenance procedure QMP 300-3, Steam Dryer Removal, did
not require Maintenance Department personnel to notify
Operating Department personnel that they were beginning to
transfer the Steam Dryer. Because of this, Operating
Department personnel were not aware that the transfer was
in progress at the time of the trip. This resulted in an
unplanned actuation of an Engineered Safety Feature (Standby
Gas Treatment System). Procedure QMP 300-3 has been revised.
No further actions are required.
(8) (closed) LER 85010, Revision 0, Unit 2: Reactor Scram and
Late Notification to NRC.
This event was discussed in Inspection Report 265/85007 and
was dispositioned as Violation. As such, no further action
is required.
(9) (open) LER 85019, P.evision 0, Unit 2: Leak Rate of All
Valves and Penetrations Exceed Technical Specifications.
This report documents that the combined leakage of all valves
and penetrations was found to be excessive during normal local
leak rate testing. Repairs and further testing was accomplished
and a supplemental report will be issued to document this upon
completion of all reviews. This LER will remain open pending
receipt of the supplemental report.
No violations or deviations were identified.
11
.
- - - ..- . - - - . -- . -- - -
!
6-
!
, .-
1. TMI Action Items-
, :(1) (closed) Item I.A.2.1 Upgrading of Reactor Operator and
i Senior Operator Training.
NRR has-issued a Safety Evaluation Report (SER) dated April 12,
f -1985 accepting the licensee's submittal to comply with this
requirement. The resident inspectors have verified that the
.
licensee's program does correspond to this submittal. 'No
! further actions are required.
(2) (closed) Item II.B.4 Training For Mitigating Core Damage
NRR has issued a SER dated April 12, 1985 accepting the
licensee's submittal to comply with this requirement. The
resident inspectors have verified that the licensee's program
( does correspond to their submittal. No further actions are
required.
'
l (3) (closed) Item II.K.3.16 Challenges and Failures of Relief
Valves
l- In a letter dated November 14, 1984, NRR accepted the licensee's
,
proposed actions concerning this item. The resident inspectors
- have confirmed that the licensee's program conforms to their
! submittal. No further actions are required.
t.
L (4) '(closed) Item II.K.3.21 Restart of Core Spray and Low Pressure
L - Coolant Injection Systems.
L
l In~a letter dated October 26, 1984, NRR agreed that no
[ modifications were warranted for Quad Cities station in
'
response to this item. No further actions are required.
(5) (closed) Item II.IK.3.24 Adequacy of Space Cooling for HPCI
and RCIC Systems. I
In a letter dated August 13, 1982, NRR found the licensee's .
submittal acceptable. The resident inspectors have verified
that the ifcensee's program complies with their submittel.
No further actions are required.
(6) (closed) Item II.IK.3.35 Effact of Loss of A-C Power on Pump
t Seals.
In a letter dated December 1, 1982, NRR agreed that no
m.odifications were warranted at Quad Cities station in
re'sponse to this item. No further actions are required.
No Violations or deviations were identified.
..
12
.
, . .. - - - _ - - ---.---- -- - . - . - . - .-
- ,;
8:
J. Regional Requests
,
(1) A problem was discovered at Byron station concerning the Main
~ Steam Isolation Valve actuators. A request was made to
determine if similar configurations existed at Quad Cities.
The resident inspectors confirmed that actuators similar to
those used at Byron were.not in use in-any applications at- ,
'
Quad Cities station.
,
(2) A request was received to inspect the licensees program
. concerning station. battery operation and maintenance. The
licensee's program was found to be acceptable with two minor
exceptions:
a) No' post-maintenance testing is performed after cell
jumpering or cell replacement. The ifcensee has agreed
to change their procedures to reflect this requirement.
b) ~ ~The station procedures for weekly and quarterly
< surveillances do not require the batteries to be on a
float charge as part of the initial' conditions. This has '
been a station practice in the past and the licensee,has
. agreed to change their procedures to reflect this '
requirement.
'
L These procedure changes will be tracked as an Open Item
i (254/85012-02(DRP) and 265/85013-02(DRP)).
No' violations or deviations were identified.
k. Followup on Headquarters Requests
l
(1) A request was received for information to support Regional >
,~
efforts in followup of Generic Letter 83-28. The requested
i information was promptly supplied. .
j' (2) A request was made of the resident inspectors to determine
i the' licensee's response to a recent safety issue concerning
'
mispositioned control rods. The inspectors verified that
procedural requirements had been written'and implemented to
ensure that'a nuclear engineer was present during' scheduled
control rod movements, to identify the conditions under which
,
the rod worth minimizer may be bypassed, to prohibit the use
- . of scram timing equipment except for testing and emergencies,
,
and to provide guidelines on the appropriate use of
" emergency-in" mode'of rod insertion and notch override switch-
'
U
in continuous' withdrawal. The inspectors also verified that
'
,
training had been provided for operators in the proper movement
. of. control' rods, the consequences of improper movement, the
- consequences
- of operating with a mispositioned rod, the
i. function of the Rod Worth Minimizer, and the scram test
l- switches.
i
4
f> ;
13
. .
,v. + ~~- , -,-a,,w,. ,n,,-e-,w,--.,-. --a _. , - ~ ,, - - .-,,-,- m n - .,-,,~,w,nvr--,,---- .,,rs,-r,-,r..-w.- -r-~ -
M
.
(3) A request was made to inspect the licensee's actions concerning
General Electric (GE) Service.Information Letter (SIL) No. 402
"Wetwell/Drywell Inerting."
\
The concern was that introduction of cold nitrogen via the
inerting system could cause cracking in vent system piping.
A review and evaluation of the design of the Quad Cities
station inerting system determined that the potential for
introduction of cold nitrogen in to the suppression chamber
was minimal. The temperature of nitrogen entering containment
is monitored and alarms in the control room on a low
temperature of 50 degrees F.
A review of past performance determined that the inerting
system has been very reliable. Procedures were also found
to be adequate, however, precautions were added to alert
operators to the problems of introducing cold nitrogen into
the system.
In response to I.E.Bulletin 84-01 both Unit suppression
chamber vent header were visually inspected. No abnormalities
were found. ,
Additionally, leakage tests are performed during each refueling
outage and repairs are performed as necessary.
No violations or deviations were identified.
1. Independent Inspection
(1) A report from Wolf Creek station reported that a security
officer, acting in a data management capacity, had entered
a command into the security computer for an emergency
evacuation. He believed the computer would reject the
command. It did not. Subsequently, a trainee in another
location verified the command as authentic without being
fully cognizant of the results of his actions. This
resulted in unlocking doors in the protected and vital
areas. The security officer immediately recognized his
error but, did not know the cancellation code, resulting
in a delay in locked condition restoration.
A report of equipment at the Quad Cities station determined
that a similar event was possible. As a result, Security
personnel are being retrained on computer procedures.
Additionally, the licensee has had the practice of assigning
no trainees to computer console duty. All operators receive
40 hours4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br /> of training first.
l
'
14
I
l
.
. - . _ - _ - - .. -
-
-
.
.
(d) A report from South Texas Project identified fabrication
interference on sway struts manufactured by NPS Industries.
It was determined that similar struts suppifed by NPS
Industries were installed at Quad Cities station. However,
their freedom of movement was verified during installation
and during a reinspection in June, 1984.
Open Items
Open items are matters which have been discussed with the ifcensee, which
will be reviewed further by the inspectors, and which involve some action
on the part of the NRC or ifcensee or both. The open items disclosed
during the inspection are discussed in Paragraphs Ib and lj.
4. Unresolved Items
Unresolved items are matter about which more information is required
in order to ascertain whether they are acceptable items, items of
noncompliance, or deviations. The unresolved item disclosed during
the inspection is discussed in Paragraph le.
5. Exit Interview
The inspectors met with licensee representatives (denoted in Paragraph 1)
throughout the month and at the conclusion of the inspection on May 31,
1985, and summariz i the scope and findings of the inspection activities.
.
The inspectors also discussed the likely informational content of the
inspection report with regard to documents or processes reviewed by the
inspectors during the inspection. The licensee did not identify any such
documents / processes as proprietary.
t *
8
15